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{{#Wiki_filter:~.CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDE)ACCESSION NSR:9603120224 DOC.DATE: 96/03/06 NOTARIZED:
{{#Wiki_filter:~     .CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM         (RIDE)
NO DOCKET I FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH.NAME AUTHOR AFFILIATION HICKEYFJ.A.
ACCESSION NSR:9603120224           DOC.DATE:   96/03/06     NOTARIZED: NO FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light DOCKET  I C 05000250 AUTH. NAME           AUTHOR AFFILIATION HICKEYFJ.A.         Florida   Power & Light Co.
Florida Power&Light Co.HOVEY,R.J.
HOVEY,R.J.           Florida   Power & Light Co.
Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION
RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 96-002-00:on 960209,automatic turbine trip/RT occurred due to high SG level.Caused by personnel error.Replaced both hinge pins on"B" SGFP discharge check valve.W/960306 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: C RECIPIENT ID CODE/NAME PD2-1 PD INTERNAL: AEOD SPD/B NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME CROTEAU,R AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB LITCO BRYCEFJ H NOAC POOREFW.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 D E N NOTE TO ALL"RIDSM RECIPIENTS:
LER   96-002-00:on 960209,automatic turbine trip/RT occurred                     C due to high SG level. Caused by personnel error. Replaced both hinge pins on "B" SGFP discharge check valve.W/960306           ltr.
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED)FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25  
DISTRIBUTION CODE: IE22T         COPIES RECEIVED:LTR         ENCL   SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT            COPIES            RECIPIENT         COPIES ID CODE/NAME         LTTR ENCL        ID CODE/NAME      LTTR ENCL PD2-1   PD               1    1      CROTEAU,R            1    1 INTERNAL: AEOD SPD/       B           2    2      AEOD/SPD/RRAB        1    1 1    1      NRR/DE/ECGB          1    1 NRR/DE/EELB                1    1      NRR/DE/EMEB          1    1 NRR/DRCH/HHFB              1    1      NRR/DRCH/HICB        1     1 NRR/DRCH/HOLB              1    1      NRR/DRCH/HQMB        1    1 NRR/DRPM/PECB              1    1      NRR/DSSA/SPLB        1    1 NRR/DSSA/SRXB              1    1      RES/DSIR/EIB         1     1 RGN2      FILE  01        1   1 D
EXTERNAL: L ST LOBBY WARD            1   1       LITCO BRYCEFJ    H  2    2 NOAC MURPHY,G.A            1   1       NOAC POOREFW.        1     1 NRC PDR                    1   1       NUDOCS FULL TXT      1     1 E
N NOTE TO ALL "RIDSM RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED)
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR             25   ENCL     25


FPL MAR06 1996 L-96-043 10 CFR 50.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.CD 20555 Gentlemen:
MAR06 1996 FPL                                                  L-96-043 10 CFR 50.73 U.S. Nuclear Regulatory Commission Attn:   Document         Control Desk Washington, D.           CD 20555 Gentlemen:
Re: Turkey Point Unit 3 Docket No.50-250 Reportable Event: 96-002-00 Au matic Turbine Tri Reactor Tri due to Hi h Steam Generator Level The attached Licensee Event Report, 250/96-002-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv).Should there be any questions, please contact us.Very truly yours, Robert J~Hov y Vice President Turkey Point Plant attachment cc: S.D.Ebneter, Regional Administrator, Region II, USNRC T-.P.Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9603120224 960306 PDR ADOCK 05000250 S PDR 3.1COSG an FPL Group company Z I]]c r kg PACILITY NAME (1)LICENSEE EVENT REPORT (LER)DOCKET NUMBER (2)PAGE (9)TURKEY POINT UNIT 3 05000250 1 OP 4 TITLE (6)AUTOMATIC TURBINE TRIP/REACTOR TRIP DUE TO HIGH STEAM GENERATOR LEVEL MON EVENT DATE (5)DAY YR LER NUMBER(6)SEQ ((RN RPT DATE (7)MON DAY OTHER PACILITIES INV.(8)PACILITY NAMES DOCKET ()(S)02 09 96 96 002 00 03 06 96 OPERATING MODE (9)POWER LEVEL (10)60 10 CFR 50.73 a 2 iv LICENSEE CONTACT FOR THIS LER (12)J.A.Hickey, Licensing Engineer Telephone Number (305)246-6668 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)SYSTEM COMPONENT MANUFACTURER NPRDS?CAUSE SYSTEM COMPONENT MANUPACTURER NPRDS?BA 65 T147 C255 SUPPLEMENTAL REPORT EXPECTED (14)NO YES 0 (if yee, coaylete EXPECTED SUBMISSION DATE)EXPECTED SUBMISSION DATE (15)MONTH DAY ABSTRACT (16)On February 09, 1996, Florida Power&Light Company's Turkey Point Unit 3 was operating in mode 1 at 60%power to support condenser waterbox cleaning.At 2329 the"B" Steam Generator Feed Pump (SGFP)was stopped to monitor its discharge check valve closing stroke.The discharge check valve did not stroke closed as expected.At 2334 the resulting feed flow transient caused the HC" Steam Generator (S/G)level to increase, resulting in a turbine trip.A reactor trip by turbine trip occurred immediately thereafter.
Re:     Turkey Point Unit         3 Docket No. 50-250 Reportable Event:           96-002-00 Au   matic Turbine Tri Reactor Tri due to Hi h Steam Generator Level The attached Licensee Event Report, 250/96-002-00,             is being provided in accordance         with 10 CFR 50.73(a) (2) (iv) .
The cause of the turbine trip/reactor trip was cognitive personnel error.The operator failed to effectively control the"CH S/G level during the feed flow transient.
Should there be any questions,             please contact us.
The NRC operations center was notified at 0035 on February 10, 1996, in accordance with 10 CFR 50.72 (b)(2)(ii), Reactor Protection System Actuation.
Very   truly yours, Robert J Hov y
LICENSEE QSNT REPORT (LER)TEXT 4TINUATION FACILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 96-002-00 PAGE NO.2 OF 4 I.'ESCRIPTION OP THE EVENT On February 09, 1996, Florida Power&Light Company's Turkey Point Unit 3 was operating in mode 1 at 60%power to support condenser waterbox cleaning.An investigation into the source of a suspected loose part in the 6B High Pressure Feedwater Heater (SN:HX)was in progress.Monitoring the , performance of each SGFP discharge check valve (SJ:V)was part of the investigation.
            ~
A pre-evolution briefing for cycling the SGFPs was conducted by on-shift supervision and a management designee.Expected plant response and potential problems were discussed, including the failure of the discharge check valve to close.The"A" SGFP (SK:P)was cycled with no abnormal indications.
Vice President Turkey Point Plant attachment cc:   S. D. Ebneter,         Regional Administrator, Region II,   USNRC T-. P. Johnson,       Senior Resident Inspector, USNRC, Turkey Point Plant 9603120224 960306 PDR   ADOCK 05000250 S                         PDR 3.1COSG Z
The diagnostic test equipment was transferred to the"B" SGFP discharge check valve and another control room pre-evolution briefing was held.At 2329 the"B" SGFP was secured.The"B" SGFP discharge check valve did not immediately close.Reverse feed flow back through the open"B" SGFP discharge check valve caused feed flow on all three S/G's to drop to approximately 1/2 of the" original flow.The operators took manual control of all three S/G Feedwater Regulating Valves (FRV)(SJ:FCV)and stabilized levels at or above approximately 38%.During this time the"B" SGFP discharge check valve slowly drifted closed and the"B" SGFP discharge MOV (SJ:ISV)closed automatically as expected.During the subsequent recovery the operator stated the"C" FRV was placed in automatic with steam flows and feed flows matched and level at program, (approximately 60%).The"A" and"B" S/G levels continued to rise above program.The operator manually reduced feed flow to stop the level increases.
an FPL Group company I]] c
This action successfully halted the level increase in the"A".and"B" S/G's.Because the"C" S/G FRV was believed to be in automatic, crew attention was focused on the"A" and"B" S/G levels.The manual decrease in feed flow for the"A" and"B" S/G's forced more flow to the"C" S/G, resulting in a level increase.The"C" S/G level was approximately 75%when the operator took manual control of the"C" FRV in an attempt to lower level.The level increase could not be stopped and direction was given for a manual reactor trip.The manual.action could not be completed before reaching the Hi-Hi S/G level turbine trip setpoint of 80%.The reactor was tripped by the turbine at 2334 as expected.The Hi-Hi S/G level trip is also a Feedwater Isolation Signal which results in an Auxiliary Feedwater (AFW)System automatic start.At 2350, while reducing Train 1 AFW flows, the"A" AFW pump (BA:P)tripped on electronic and mechanical overspeed.
 
Unit 3 was stabilized at no-load conditions and the Emergency Operating Procedures were exited approximately 15 minutes later at 0005 on February 10, 1996.At 0200 on February 10, 1996, the"C" AFW Pump was realigned to restore Train 1 AFW System operability.
r kg
LICENSEE EST REPORT (LER)TEXT MTIEUATIOE FAC,ILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 96-002-00 PAGE NO.3 OF 4 II.CAUSE OP THE EVENT Root Cause The root cause of the event was cognitive personnel error.The>>C>>S/G FRV was placed in automatic control and acceptable controlling performance was not verified.With the>>C>>FRV in automatic, the operator's attention was diverted to other plant parameters.
 
Required operator actions to compensate for the subsequent increase in>>C>>S/G level did not occur.Contributin Cause The>>B>>SGFP discharge check valve failed to close as expected.The cause of the slow closure, was the failure of tack welds on one of the hinge pin retaining bolts.The retaining bolt unscrewed, which allowed the hinge pin to fall out.>>A>>AFW Pum Overs eed The>>A>>AFW Pump tripped on electronic and mechanical overspeed due to binding of the governor.The cause of the binding was pitting on the governor stem, induced by environmental corrosion.
LICENSEE EVENT REPORT                                                       (LER)
III.ANALYSIS OP THE EVENT The Updated Final Safety Analysis Report (UFSAR)analysis assumes a loss of normal feedwater to'll steam generators due to the loss of'he feedwater pumps or valve malfunction.
PACILITY NAME (1)                                                                                      DOCKET NUMBER (2)     PAGE (9)
In the February 09 event, feed flow was not lost completely, but was significantly reduced.All steam generators were initially affected by the reduction in feedwater flow.In the analysis, the reactor trip is expected to occur due to a Low-Low Level in any steam generator or Steam/Feedwater Flow Mismatch Coincident with Low Level in any steam generator.
TURKEY POINT UNIT 3                                               05000250               1     OP     4 TITLE (6)           AUTOMATIC TURBINE TRIP/REACTOR TRIP DUE TO HIGH STEAM GENERATOR LEVEL EVENT DATE   (5)         LER NUMBER(6)           RPT DATE (7)             OTHER PACILITIES INV. (8)
In this event neither trip occurred due to operator actions which stabilized the S/G levels above the Low and Low-Low Level setpoints~The analysis shows that following a loss of normal feedwater, AFW is capable of removing the stored and residual heat, thus preventing either overpressurization of the reactor coolant system or loss of water from the reactor core.The analysis also assumes only one AFW pump is available due to a single failure.Two AFW pumps were available following the overspeed of the>>A>>AFW pump, therefore, the plant's response was bounded by the analysis.This event did not compromise the health or safety of plant personnel or the general public.This event is reportable under the requirements of 10 CFR 50.73(a)(2)(iv).
MON          DAY      YR                  SEQ ((    RN    MON    DAY                            PACILITY NAMES               DOCKET () (S) 02           09     96           96     002       00     03     06     96 OPERATING MODE   (9)
LICENSEE IDENT REPORT (LER)TEXT (TINUATION FACILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 96-002-00 PAGE NO.4 OF 4 IV.CORRECTIVE ACTIONS 1.Both hinge pins on the"B" SGFP discharge check valve have been replaced.The new tack welds on the retaining bolts have been verified as adequately sized.The"A" SGFP discharge check valve was inspected and reassembled, the retaining bolt tack welds'have been verified as adequately sized.All similar check valves regardless of application have been or will be inspected for adequately sized retaining bolt tack welds.2.Remedial simulator training was conducted for the individual controlling the"C" S/G level.The conditions of the event were approximately duplicated and the individual successfully controlled the S/G level.3.The governor stem on the"A" AFW Pump has been replaced.A special surveillance for stroking the governor stems is in place.When the AFW Pump governor stems are replaced with an upgraded corrosion resistant stem, the special surveillance will be discontinued.
POWER LEVEL (10)           60 10 CFR     50.73 a         2     iv LICENSEE CONTACT FOR THIS LER (12)
4.The NC" S/G Flow Control Valve performance in automatic was investigated.
Telephone Number J. A. Hickey, Licensing Engineer (305) 246-6668 COMPLETE ONE           LINE     FOR EACH COMPONENT FAILURE DESCRIBED                           IN THIS       REPORT     (13)
The results of the investigation revealed no abnormalities with the"C" S/G flow control valve.5.Operations management will review this event with each operating crew.a.The Nuclear Plant Supervisor involved in this event has completed a Command and Control performance evaluation of the event.6~Training will review/establish scenarios which approximate this event.7.A Post-Trip meeting was held and video taped.In attendance were approximately 65 individuals from Operations, Training, Site Management and the President of the Nuclear Division.The meeting format was an"open forum" to ensure all parties understood the event.The meeting provided a vehicle to clearly reenforce Management's expectation that prompt manual action, including a manual reactor trip must be taken prior to challenging any automatic plant protective feature.V.ADDITIONAL INFORMATION A similar SGFP discharge check valve failure occurred on Unit 4 in 1993.A turbine trip/reactor trip on Hi-Hi S/G level occurred on Unit 4 in 1993.The cause was improperly valving in a high pressure feedwater heater.}}
SYSTEM         COMPONENT   MANUFACTURER             NPRDS?     CAUSE       SYSTEM       COMPONENT   MANUPACTURER     NPRDS?
BA           65               T147 C255 SUPPLEMENTAL REPORT EXPECTED     (14)   NO             YES 0                                   EXPECTED SUBMISSION MONTH        DAY DATE (15)
(if yee, coaylete  EXPECTED SUBMISSION DATE)
ABSTRACT (16)
On   February 09, 1996, Florida Power & Light Company's Turkey Point Unit 3 was operating in mode 1 at 60% power to support condenser waterbox cleaning.
At 2329 the "B" Steam Generator Feed Pump (SGFP) was stopped to monitor its discharge check valve closing stroke. The discharge check valve did not stroke closed as expected. At 2334 the resulting feed flow transient caused the HC" Steam Generator (S/G) level to increase, resulting in a turbine trip. A reactor trip by turbine trip occurred immediately thereafter.
The cause         of the turbine trip/reactor trip                         was   cognitive personnel error. The operator failed to effectively control the                                 "CH   S/G level during the feed flow transient.
The NRC       operations center                 was   notified at       0035 on February 10, 1996,                     in accordance with     10 CFR       50.72 (b) (2)             (ii),   Reactor Protection System Actuation.
 
LICENSEE QSNT REPORT             (LER) TEXT 4TINUATION FACILITY NAME               DOCKET NUMBER            LER NUMBER            PAGE NO.
TURKEY POINT UNIT 3             05000250               96-002-00             2 OF 4 I.'ESCRIPTION     OP THE EVENT On February 09, 1996, Florida Power       & Light Company's Turkey Point Unit 3 was operating in   mode 1 at 60% power to support condenser waterbox cleaning.
An investigation into the source of a suspected loose part in the 6B High Pressure Feedwater Heater (SN:HX) was in progress.             Monitoring the
,   performance of each SGFP discharge check valve (SJ:V) was part of the investigation. A pre-evolution briefing for cycling the SGFPs was conducted by on-shift supervision and a management designee.             Expected plant response and potential problems were discussed, including the failure of the discharge check valve to close.
The "A" SGFP (SK:P) was cycled with no abnormal indications.             The diagnostic test equipment was transferred to the "B" SGFP discharge check valve             and another control room pre-evolution briefing was held. At 2329 the "B" SGFP was secured.     The "B" SGFP discharge check valve did not immediately close.
Reverse feed flow back through the open "B" SGFP discharge check valve caused feed flow on all three S/G's to drop to approximately 1/2 of the
  "
original flow. The operators took manual control             of all three S/G Feedwater Regulating Valves (FRV) (SJ:FCV) and stabilized levels at or above approximately 38%. During this time the "B" SGFP discharge check valve slowly drifted closed and the "B" SGFP discharge MOV (SJ:ISV) closed automatically as expected.
During the subsequent recovery the operator stated the "C" FRV was placed in automatic with steam flows and feed flows matched and level at program, (approximately 60%). The "A" and "B" S/G levels continued to rise above program. The operator manually reduced feed flow to stop the level increases.     This action successfully halted the level increase in the "A".
and "B" S/G's.       Because the "C" S/G FRV was believed to be in automatic, crew attention was focused on the "A" and "B" S/G levels. The manual decrease in feed flow for the "A" and "B" S/G's forced more flow to the "C" S/G, resulting in a level increase.         The "C" S/G level was approximately 75%
when the operator took manual control of the "C" FRV in an attempt to lower level. The level increase could not be stopped and direction was given for a manual reactor trip. The manual. action could not be completed before reaching the Hi-Hi S/G level turbine trip setpoint of 80%.
The reactor was tripped by the turbine at 2334 as expected. The Hi-Hi S/G level trip is also a Feedwater Isolation Signal which results in an Auxiliary Feedwater (AFW) System automatic start. At 2350, while reducing Train 1 AFW flows, the "A" AFW pump (BA:P) tripped on electronic and mechanical overspeed.
Unit   3 was stabilized at no-load conditions       and the Emergency Operating Procedures were exited approximately 15 minutes           later at 0005 on February 10, 1996.
At 0200 on February 10, 1996, the "C"           AFW Pump was   realigned to restore Train 1 AFW System operability.
 
LICENSEE   EST       REPORT   (LER) TEXT MTIEUATIOE FAC,ILITY NAME                   DOCKET NUMBER          LER NUMBER              PAGE NO.
TURKEY POINT UNIT 3                 05000250             96-002-00                 3 OF 4 II. CAUSE OP THE EVENT Root Cause The   root cause of the event was cognitive personnel error. The >>C>> S/G FRV was   placed in automatic control and acceptable controlling performance was not verified. With the >>C>> FRV in automatic, the operator's attention was diverted to other plant parameters. Required operator actions to compensate for the subsequent increase in >>C>> S/G level did not occur.
Contributin       Cause The >>B>> SGFP       discharge check valve failed to close as expected. The of the slow closure, was the failure of tack welds on one of the hingecause retaining bolts. The retaining bolt unscrewed, which allowed the hinge pin              pin to fall out.
>>A>> AFW Pum       Overs eed The >>A>> AFW Pump       tripped   on electronic and mechanical overspeed due to binding of the governor.           The cause of the binding was pitting on the governor stem, induced by environmental corrosion.
III. ANALYSIS OP       THE EVENT The Updated Final Safety Analysis Report (UFSAR) analysis assumes a loss of normal feedwater       to'll pumps or valve malfunction.
steam generators due to the loss of'he feedwater In the February 09           feed flow was not lost completely, but was significantly reduced. event,        All steam generators were initially affected by the reduction in feedwater flow. In the reactor trip is expected to occur due to a Low-Low Level in any analysis,      steam the generator or Steam/Feedwater Flow Mismatch Coincident with Low Level in any steam generator.         In this event neither trip occurred due to operator actions which stabilized the S/G levels above the Low and Low-Low Level setpoints     ~   The analysis shows that following a loss of normal feedwater, AFW is capable of removing the stored and residual heat, thus preventing either overpressurization of the reactor coolant system or loss of water from the reactor core. The analysis also assumes only one AFW pump is available       due to a single failure.     Two AFW pumps were   available following the overspeed of the >>A>> AFW pump, therefore, the plant's response was bounded by the analysis.           This event did not compromise the health or safety of plant personnel or the general public.
This event is reportable under the requirements of             10 CFR   50.73(a) (2) (iv) .
 
LICENSEE IDENT REPORT           (LER) TEXT (TINUATION FACILITY NAME                   DOCKET NUMBER          LER NUMBER              PAGE NO.
TURKEY POINT UNIT 3               05000250             96-002-00               4 OF 4 IV. CORRECTIVE ACTIONS
: 1. Both hinge pins on the "B" SGFP discharge check valve have been replaced. The new tack welds on the retaining bolts have been verified as adequately sized. The "A" SGFP discharge check valve was inspected and reassembled, the retaining bolt tack welds 'have been verified as adequately sized. All similar check valves regardless of application have been or will be inspected for adequately sized retaining bolt tack welds.
: 2. Remedial simulator training was conducted for the individual controlling the "C" S/G level. The conditions of the event were approximately duplicated and the individual successfully controlled the S/G level.
: 3. The governor stem on the "A"         AFW Pump has been replaced. A special surveillance for stroking the governor stems is in place. When the AFW Pump governor stems are replaced with an upgraded corrosion resistant stem, the special surveillance will be discontinued.
: 4. The     NC" S/G Flow   Control Valve performance in automatic     was investigated. The results of the investigation revealed no abnormalities with the "C" S/G flow control valve.
: 5. Operations management will review this event with each operating crew.
: a.     The Nuclear Plant Supervisor involved in this event has completed a Command and Control performance evaluation of the event.
6 ~ Training will review/establish scenarios which approximate this event.
: 7. A Post-Trip meeting was held and video taped.             In attendance were approximately 65 individuals from Operations, Training, Site Management and the President of the Nuclear Division. The meeting format was an "open forum" to ensure all parties understood the event. The meeting provided a vehicle to clearly reenforce Management's expectation that prompt manual action, including a manual reactor trip must be taken prior to challenging any automatic plant protective feature.
V. ADDITIONAL INFORMATION A   similar   SGFP   discharge check valve   failure occurred   on Unit 4 in 1993.
A   turbine trip/reactor trip on Hi-Hi S/G       level occurred on Unit 4 in 1993. The cause was improperly valving in a high pressure             feedwater heater.}}

Revision as of 08:22, 22 October 2019

LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr
ML17353A586
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 03/06/1996
From: Jim Hickey, Hovey R
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-96-043, L-96-43, LER-96-002, LER-96-2, NUDOCS 9603120224
Download: ML17353A586 (8)


Text

~ .CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDE)

ACCESSION NSR:9603120224 DOC.DATE: 96/03/06 NOTARIZED: NO FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light DOCKET I C 05000250 AUTH. NAME AUTHOR AFFILIATION HICKEYFJ.A. Florida Power & Light Co.

HOVEY,R.J. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 96-002-00:on 960209,automatic turbine trip/RT occurred C due to high SG level. Caused by personnel error. Replaced both hinge pins on "B" SGFP discharge check valve.W/960306 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 CROTEAU,R 1 1 INTERNAL: AEOD SPD/ B 2 2 AEOD/SPD/RRAB 1 1 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 D

EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCEFJ H 2 2 NOAC MURPHY,G.A 1 1 NOAC POOREFW. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 E

N NOTE TO ALL "RIDSM RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED)

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MAR06 1996 FPL L-96-043 10 CFR 50.73 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. CD 20555 Gentlemen:

Re: Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 96-002-00 Au matic Turbine Tri Reactor Tri due to Hi h Steam Generator Level The attached Licensee Event Report, 250/96-002-00, is being provided in accordance with 10 CFR 50.73(a) (2) (iv) .

Should there be any questions, please contact us.

Very truly yours, Robert J Hov y

~

Vice President Turkey Point Plant attachment cc: S. D. Ebneter, Regional Administrator, Region II, USNRC T-. P. Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9603120224 960306 PDR ADOCK 05000250 S PDR 3.1COSG Z

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LICENSEE EVENT REPORT (LER)

PACILITY NAME (1) DOCKET NUMBER (2) PAGE (9)

TURKEY POINT UNIT 3 05000250 1 OP 4 TITLE (6) AUTOMATIC TURBINE TRIP/REACTOR TRIP DUE TO HIGH STEAM GENERATOR LEVEL EVENT DATE (5) LER NUMBER(6) RPT DATE (7) OTHER PACILITIES INV. (8)

MON DAY YR SEQ (( RN MON DAY PACILITY NAMES DOCKET () (S) 02 09 96 96 002 00 03 06 96 OPERATING MODE (9)

POWER LEVEL (10) 60 10 CFR 50.73 a 2 iv LICENSEE CONTACT FOR THIS LER (12)

Telephone Number J. A. Hickey, Licensing Engineer (305) 246-6668 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

SYSTEM COMPONENT MANUFACTURER NPRDS? CAUSE SYSTEM COMPONENT MANUPACTURER NPRDS?

BA 65 T147 C255 SUPPLEMENTAL REPORT EXPECTED (14) NO YES 0 EXPECTED SUBMISSION MONTH DAY DATE (15)

(if yee, coaylete EXPECTED SUBMISSION DATE)

ABSTRACT (16)

On February 09, 1996, Florida Power & Light Company's Turkey Point Unit 3 was operating in mode 1 at 60% power to support condenser waterbox cleaning.

At 2329 the "B" Steam Generator Feed Pump (SGFP) was stopped to monitor its discharge check valve closing stroke. The discharge check valve did not stroke closed as expected. At 2334 the resulting feed flow transient caused the HC" Steam Generator (S/G) level to increase, resulting in a turbine trip. A reactor trip by turbine trip occurred immediately thereafter.

The cause of the turbine trip/reactor trip was cognitive personnel error. The operator failed to effectively control the "CH S/G level during the feed flow transient.

The NRC operations center was notified at 0035 on February 10, 1996, in accordance with 10 CFR 50.72 (b) (2) (ii), Reactor Protection System Actuation.

LICENSEE QSNT REPORT (LER) TEXT 4TINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY POINT UNIT 3 05000250 96-002-00 2 OF 4 I.'ESCRIPTION OP THE EVENT On February 09, 1996, Florida Power & Light Company's Turkey Point Unit 3 was operating in mode 1 at 60% power to support condenser waterbox cleaning.

An investigation into the source of a suspected loose part in the 6B High Pressure Feedwater Heater (SN:HX) was in progress. Monitoring the

, performance of each SGFP discharge check valve (SJ:V) was part of the investigation. A pre-evolution briefing for cycling the SGFPs was conducted by on-shift supervision and a management designee. Expected plant response and potential problems were discussed, including the failure of the discharge check valve to close.

The "A" SGFP (SK:P) was cycled with no abnormal indications. The diagnostic test equipment was transferred to the "B" SGFP discharge check valve and another control room pre-evolution briefing was held. At 2329 the "B" SGFP was secured. The "B" SGFP discharge check valve did not immediately close.

Reverse feed flow back through the open "B" SGFP discharge check valve caused feed flow on all three S/G's to drop to approximately 1/2 of the

"

original flow. The operators took manual control of all three S/G Feedwater Regulating Valves (FRV) (SJ:FCV) and stabilized levels at or above approximately 38%. During this time the "B" SGFP discharge check valve slowly drifted closed and the "B" SGFP discharge MOV (SJ:ISV) closed automatically as expected.

During the subsequent recovery the operator stated the "C" FRV was placed in automatic with steam flows and feed flows matched and level at program, (approximately 60%). The "A" and "B" S/G levels continued to rise above program. The operator manually reduced feed flow to stop the level increases. This action successfully halted the level increase in the "A".

and "B" S/G's. Because the "C" S/G FRV was believed to be in automatic, crew attention was focused on the "A" and "B" S/G levels. The manual decrease in feed flow for the "A" and "B" S/G's forced more flow to the "C" S/G, resulting in a level increase. The "C" S/G level was approximately 75%

when the operator took manual control of the "C" FRV in an attempt to lower level. The level increase could not be stopped and direction was given for a manual reactor trip. The manual. action could not be completed before reaching the Hi-Hi S/G level turbine trip setpoint of 80%.

The reactor was tripped by the turbine at 2334 as expected. The Hi-Hi S/G level trip is also a Feedwater Isolation Signal which results in an Auxiliary Feedwater (AFW) System automatic start. At 2350, while reducing Train 1 AFW flows, the "A" AFW pump (BA:P) tripped on electronic and mechanical overspeed.

Unit 3 was stabilized at no-load conditions and the Emergency Operating Procedures were exited approximately 15 minutes later at 0005 on February 10, 1996.

At 0200 on February 10, 1996, the "C" AFW Pump was realigned to restore Train 1 AFW System operability.

LICENSEE EST REPORT (LER) TEXT MTIEUATIOE FAC,ILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY POINT UNIT 3 05000250 96-002-00 3 OF 4 II. CAUSE OP THE EVENT Root Cause The root cause of the event was cognitive personnel error. The >>C>> S/G FRV was placed in automatic control and acceptable controlling performance was not verified. With the >>C>> FRV in automatic, the operator's attention was diverted to other plant parameters. Required operator actions to compensate for the subsequent increase in >>C>> S/G level did not occur.

Contributin Cause The >>B>> SGFP discharge check valve failed to close as expected. The of the slow closure, was the failure of tack welds on one of the hingecause retaining bolts. The retaining bolt unscrewed, which allowed the hinge pin pin to fall out.

>>A>> AFW Pum Overs eed The >>A>> AFW Pump tripped on electronic and mechanical overspeed due to binding of the governor. The cause of the binding was pitting on the governor stem, induced by environmental corrosion.

III. ANALYSIS OP THE EVENT The Updated Final Safety Analysis Report (UFSAR) analysis assumes a loss of normal feedwater to'll pumps or valve malfunction.

steam generators due to the loss of'he feedwater In the February 09 feed flow was not lost completely, but was significantly reduced. event, All steam generators were initially affected by the reduction in feedwater flow. In the reactor trip is expected to occur due to a Low-Low Level in any analysis, steam the generator or Steam/Feedwater Flow Mismatch Coincident with Low Level in any steam generator. In this event neither trip occurred due to operator actions which stabilized the S/G levels above the Low and Low-Low Level setpoints ~ The analysis shows that following a loss of normal feedwater, AFW is capable of removing the stored and residual heat, thus preventing either overpressurization of the reactor coolant system or loss of water from the reactor core. The analysis also assumes only one AFW pump is available due to a single failure. Two AFW pumps were available following the overspeed of the >>A>> AFW pump, therefore, the plant's response was bounded by the analysis. This event did not compromise the health or safety of plant personnel or the general public.

This event is reportable under the requirements of 10 CFR 50.73(a) (2) (iv) .

LICENSEE IDENT REPORT (LER) TEXT (TINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY POINT UNIT 3 05000250 96-002-00 4 OF 4 IV. CORRECTIVE ACTIONS

1. Both hinge pins on the "B" SGFP discharge check valve have been replaced. The new tack welds on the retaining bolts have been verified as adequately sized. The "A" SGFP discharge check valve was inspected and reassembled, the retaining bolt tack welds 'have been verified as adequately sized. All similar check valves regardless of application have been or will be inspected for adequately sized retaining bolt tack welds.
2. Remedial simulator training was conducted for the individual controlling the "C" S/G level. The conditions of the event were approximately duplicated and the individual successfully controlled the S/G level.
3. The governor stem on the "A" AFW Pump has been replaced. A special surveillance for stroking the governor stems is in place. When the AFW Pump governor stems are replaced with an upgraded corrosion resistant stem, the special surveillance will be discontinued.
4. The NC" S/G Flow Control Valve performance in automatic was investigated. The results of the investigation revealed no abnormalities with the "C" S/G flow control valve.
5. Operations management will review this event with each operating crew.
a. The Nuclear Plant Supervisor involved in this event has completed a Command and Control performance evaluation of the event.

6 ~ Training will review/establish scenarios which approximate this event.

7. A Post-Trip meeting was held and video taped. In attendance were approximately 65 individuals from Operations, Training, Site Management and the President of the Nuclear Division. The meeting format was an "open forum" to ensure all parties understood the event. The meeting provided a vehicle to clearly reenforce Management's expectation that prompt manual action, including a manual reactor trip must be taken prior to challenging any automatic plant protective feature.

V. ADDITIONAL INFORMATION A similar SGFP discharge check valve failure occurred on Unit 4 in 1993.

A turbine trip/reactor trip on Hi-Hi S/G level occurred on Unit 4 in 1993. The cause was improperly valving in a high pressure feedwater heater.