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{{Adams | |||
| number = ML20151T203 | |||
| issue date = 08/05/1988 | |||
| title = Insp Rept 50-155/88-13 on 880602-0718.Violations Noted.Major Areas Inspected:Surveillance Observation of Pressure Test on NSSS & Reactor Depressurization Sys & Security Observations Re Day to Day Plant Activities | |||
| author name = Jackiw I | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000155 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-155-88-13, IEB-88-005, IEB-88-007, IEB-88-5, IEB-88-7, NUDOCS 8808160287 | |||
| package number = ML20151T187 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 8 | |||
}} | |||
See also: [[see also::IR 05000155/1988013]] | |||
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U.S. NUCLEAR REGULATORY COMMISSION | |||
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REGION III I | |||
f | |||
hport No. 50-155/88013(DRP) | |||
Docket No. 50-155 License No. DPR-6 | |||
Licensee: Consumers Power Company | |||
212 West Michigan Avenue | |||
Jackson, MI 49201 | |||
Facility Name: Big Rock Point Nu ear Plant | |||
Inspection At: Charlevoix, MI 49720 | |||
Inspection Conducted: June 2 through July 18, 1988 , | |||
Inspector: E. Plettner 8'd 7N | |||
Uate | |||
Inspector: N. Williamsen . | |||
Date | |||
t | |||
Approved By: 1 N ! | |||
ReactorPyojectsSection28 Date | |||
Inspection Summary | |||
Inspection on June 2 through July 18,1988 (Report No. 50-155/88-013(DRP)) | |||
Areas Inspected: The inspection was routine, unannounced, and conducted by- | |||
the Senior Resident Inspector and the Resident Inspector. The functional ' | |||
areas inspected consisted of the followina areas. Surveillance observation | |||
of the pressure test on the nuclear steam supply system and the reactor | |||
depressurization system. Maintenance observation of work performed on | |||
motor operated isolation valves and the reinstallation of the reactor | |||
depressurization valves. Operational safety verification, radiological | |||
, | |||
practices, and security observations involving day to day plant activities. | |||
Startup/ refuel activities associated with the refuel and startup of the | |||
reactor. NRC Bulletins on defective piping material and pover oscillations | |||
4 | |||
ir, boiling water reactors. | |||
Results: The licensee has demonstrated a desire to respond in a timely | |||
manner to issues and concerns presented to them by the NRC. The surveillance, | |||
maintenanca, operational safety, radiological program, and the security | |||
program appeared to ensure public health and safety. Two violations were | |||
, | |||
identified in this report. The violation in the maintenance section | |||
addresses inadequate quality controls and the violation in the operational | |||
safety section addresses the failure to follow procedure when using a copy | |||
- | |||
of a controlled document. | |||
8808160287 880805 | |||
gDR ApoCK 05000155 ' | |||
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DETAILS | |||
1. Persons Contacted | |||
*T. Elward, Plant Superintendent | |||
*A. Pet'tjean, Planni:ig and Administrative Services | |||
Superintendent | |||
G. Withrow, Engineering Maintenance Superintendent | |||
*R. Alexander Technical Engineer | |||
L. Monshor, Quality As:urance Superintendent | |||
*J. Seer, Chemistry / Health Physics Superintendent | |||
*R. Scheels, ' Acting Operations Supervisor | |||
"R. Hill, Sr. QA Consultant | |||
*P. Donnelly, Nuclear Assurance Administrator | |||
*R. Schrader, E & M Superintendent, Acting . | |||
*M. Bielinski, Production and Plant Performance, | |||
Superintendent, Acting | |||
*T. Hagan, Director Nuclear Training | |||
The inspector a'.so contacted other licensee personnel in the Operations, | |||
Maintenance, Radiation Protection, and Technical Departments. | |||
* Denotes those present at exit interview. | |||
2. Monthly Surveillance Observation (61726) | |||
The NRC inspectors observed Technical Specification required surveillance | |||
tests. The reviews and observations were conducted to verify that facility | |||
surveillance operations were performed in accordance with the requirements | |||
established in the Operating License and Technical Specification. | |||
The Senior Resident Inspector (SRI) observed the licensee's performance | |||
of the following surveillance tests on the indicated dates: | |||
June 20, 1988, TV-10, "Pressure Test of Nuclear Steam Supply System," | |||
Revision 37, dated June 14, 1988, with approved. temporary changes to | |||
allow the use of a new hydro test pump. A failed relief valve in the | |||
Reactor Water Clean-up System was noted during the test. A maintenance | |||
work order was issued and a new valve installed. The licensee also | |||
replaced two other relief valves in the system since they were the same | |||
age as the failed valve. A second test was performed and observed by | |||
the SRI on June 22, 1988, with satisfactory results. | |||
July 13,1988, T30-30, "RDS Cabinet Test (Sensor Cabinet C/ Actuation | |||
Cabinet 3)," Revision 24, dated January 11, 1988. The procedure was | |||
satisfactorily performed by a licensed operator and an auxiliary | |||
operator. | |||
No violations or deviations were identified in this area. | |||
2 | |||
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3. Monthly Maintenance Observation ' ?703) | |||
Station maintenance activities of safety related systems and components | |||
listed below were observed / reviewed to ascertain that they were conducted | |||
in accordance with approved procedures, regulatory guides and industry | |||
codes or standards and in conformance with technical specifications. | |||
The following items were considered during this review: the limiting . | |||
conditions for operation were met while components or systems were removed | |||
from service; approvals were obtained prior to initiating the work; | |||
activities were accomplished using approved procedures and were inspected | |||
as applicable; functional testing ond/or calibrations were performed prior | |||
to returning components or systems to service; quality control records | |||
were maintained; activities were accomplished by qual fied personnel; | |||
parts and materials used were properly certified; radiological controls | |||
were implemented; and fire prevention controls were implemented. | |||
Work requests were reviewed to determine status of outstanding jobs and to | |||
assure that priority is assigned to safety-related equipment maintenance | |||
which may affect system performance. | |||
On June 18, 1988, the SRI observed the performance of maintenance on | |||
motor operated Valve IA-760 under Work Request 88-PCS-0075. | |||
The SRI reviewed the certification test reports of the Reactor | |||
Depressurization System Valves from Wyle Laboratory. The certification | |||
reports identified each main valve and its associated pilot valve, the | |||
full-stroke time, the leak rates, acceptance criteria, and test proceoure | |||
used to perform the test. Pilot valve assembly number one failed the test | |||
on the first attempt. Repairs were made and testing was conducted with | |||
the second test results being satisfactory. The certificate numbers were | |||
49294-1, -2, -3, and -4. The SRI observed the installation of the valves | |||
on June 24 and 25, 1988, under Maintenance Work Orders 88-RDS-065 and 066. | |||
During the refueling / maintenance outage the licensee replaced the | |||
diaphragms in the Control Rod Drive Scram Valves (CRDSV), a safety-related | |||
system. All 64 valve diaphragms were replaced and tested for proper | |||
operation. It was during post maintenance testing that personnel | |||
discovered excessive air leakage from the valves. The licensee | |||
investigated the problem and found that the diaphragms had been installed | |||
upside down and, in addition, four of the 64 diaphragms had been | |||
incorrectly manufactured resulting in failure of the diaphragms. | |||
Subsequently, all 64 diaphragms, manufactured by Hammel-Dahl, were replaced | |||
for a second time. The licensee sent a letter to General Electric and the | |||
Boiling Water Reactor Owner's Group to inform them of the possible | |||
defective diaphragms. Big Rock Point was one of the first plants to | |||
replace these diaphragms because of General Electric's Service Information | |||
Letter No. 457. The SRI inquired into the amount of Quality Control (QC) | |||
provided during the maintenance activity. The results of the inquiry | |||
revealed that QC had reviewed the purchase agreement documents before work | |||
and work completion documents. During the first installation performed in | |||
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April and May.1988, of the 64 diaphragms, no member'of:the plant's QC | |||
organization observed the activity through one complete disassembly, | |||
repai*, and reassembly process. No inspection was performed to include a | |||
dimensional. check of the diaphragms or a comparison between diaphragms fcr | |||
consistency. The failure to inspect installation activities.and perform | |||
measurements or tests of material ~ is an apparent violation of quality . | |||
control requirements of 10 CFR 50, . Appendix B, Criterion X, as implemented | |||
by Big Rock Point's, "Quality Assurance Description for Operational Nuclear | |||
Power Plants," as described in Section 10. (155/88013-01). | |||
Work on the CRDSVs was performed by Consumers Power Company's traveling , | |||
maintenance crew who had their own supervisor. Training was conducted | |||
for the crew prior to allowing work to commence on the CRDSV. Corrective | |||
actions taken b/ the licensee prior to the second installation in June | |||
1988, were to revise the installation procedure, and have a plant QC | |||
individual observe at least one complete installation, The SRI verified | |||
by record review and interview that the licensee implemented the | |||
corrective actions. Full-stroke testing proved operability of the CRDSV. | |||
This problem resulted in an extended outage, a great deal of rework and | |||
testing, and additional cost to purchase the replacement parts. | |||
One violation was identified in this area. | |||
4. Operational Safety Verification (71707) | |||
The inspector observed control room operations, reviewed applicable | |||
logs, and conducted discussions with control room operators-during the | |||
inspection period. The inspector verified the operability of selected | |||
emergency systems, reviewed tagout records, and verified proper return | |||
to service of affected components. Tours of the containment sphere and | |||
turbine building were conducted to observe plant equipment conditions, | |||
including potential fire hazards, fluid leaks, and excessive vibrations | |||
and to verify that maintenance requests had been initiated for equipment | |||
in need of maintenance. The inspector observed plant housekeeping / | |||
cleanliness conditions and controls. During the. inspection period, | |||
the inspector walked down the accessible portions of the Reactor. | |||
Depressurization Post Incident, Core Spray, and Containment Spray | |||
systems to. verify operability. | |||
During plant tours conducted this period, the SRI noted that. copies of the | |||
controlled documents used to direct safety activities listed below were | |||
found at their associated work site without being marked "Working Copy" | |||
or "Working Controlled Copy," on the date shown: | |||
* | |||
June 18, 1988: System Operating Procedures (S0P) 19, "Make up | |||
System," Revision 140. | |||
June 21, 1988: S0P 15, "Condensate System," Revision 94. | |||
June 21, 1988: 50P 11, "Radioactive Waste System," Revision 117. | |||
July 6, 1988: Administrative Procedure 4.2.1, "Material | |||
Control," Revision 4. | |||
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10 CFR 50, Appendix B, Criterion V, as implemented by Big Rock Point's, | |||
"Quality Assurance Program Description for Operational Nucle'ar Power | |||
Plants," as described in Section 5.0, requires that activities affecting | |||
quality shall be prescribed by documented procedures. Administrative | |||
Procedure 4.1.8 "Procedure Assurance," Revision 1, dated February 12, 1988, | |||
Section 12.0 titled "Short Term Controlled Documents," requires that | |||
controlled documents needed as working level procedures shall be clearly | |||
marked "Working Copy" or "Working Controlled Copy." Failure of the three | |||
working SOP's and the working Administrative Procedure to be marked | |||
"Working Cr,sy" or "Working Controlled Copy," is an apparent violation. | |||
(155/88013-02). | |||
One violation was identified in this area. | |||
5. Radiological Protection Observations (71709) | |||
The NRC inspectors verified that-selected activities of the licensee's - | |||
radiological protection program were. implemented in compliance with | |||
the facility policies, procedures, and regulatory requirements. The | |||
activities observed and/or reviewed during this inspection period were | |||
that health physics (HP) supervisory personnel were conducting plant tours | |||
to check on activities in progress. Radiation work permits contained the | |||
appropriate information to ensure work was performed in a safe and | |||
controlled manner. Personnel in radiation controlled areas (RCA) were | |||
wearing the required personnel monitoring equipment and protective | |||
clothing. Radiation and/or contamir.sted areas were properly posted and | |||
controlled based on the activity levels within the area. Personnel | |||
properly frisked prior to exiting an RCA. | |||
No violations or deviations were identified in this area. | |||
6. Security Observations (71881) | |||
The NRC Inspectors verified by observation or record review that physical | |||
security measures were being implemented as prescribed in the licensee's | |||
approved physical security plan. The elements contained in the inspection , | |||
were security manning requirements, access control of both personnel and' ! | |||
vehicles, and detection / assessment aids. Throughout the inspection | |||
period, the inspectors observed that personnel within the protected area ) | |||
(PA) properly displayed their identification badges. Vehicles were ' | |||
properly authorized, searcheu, and escorted or controlled within the PA. | |||
Persons and packages were properly checked and cleared before entry into | |||
the PA. When security equipment failure or impairment occurred the 1 | |||
required compensatory measures were empluyed. Security force actions ! | |||
were conducted in a professional manner. ' | |||
No violations or deviations were identified in this area. | |||
7. Startup Testing - Refueling (72700) | |||
On June 11, 1988, during refueling operations the licensee found that a l | |||
fuel bundle could not be placed into the position required by the fuel ! | |||
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load sequence Procedure TR-46. . Fuel loading activities were stopped until | |||
the problem could be resolved. The reactor had been verified subcritical | |||
throughout the performance of the procedure. Core verification was | |||
performed with a TV camera to ensure all remaining fuel bundles were | |||
correctly loaded. No other bundles were found out of position. The | |||
reactor engineer made the necessary temporary changes, with approval, to | |||
the fuel load sequence procedure to place the misplaced bundle into.its | |||
correct position. The remaining steps of the procedure were completed | |||
without further problems. Final core verification was performed | |||
satisfactorily. The. licensee will be performing an' evaluation to | |||
determine the root cause and recommend actions to prevent reoccurrence. | |||
This apparent violation of the fuel load sequence procedure will not be | |||
issued because it appears to meet the five criteria stated in 10 CFR 2, | |||
Appendix C (V), Section G.1: (a) it was identified by the licensee; | |||
(b) it fits in Severity Level IV or V; (c) it was reported, if required; | |||
(d) It is being corrected including measures to prevent recurrence, within | |||
a reasonable time; and (e) it was not a violation that could reasonably be | |||
expected to have been prevented by the licensee's corrective action for a | |||
previous violation. | |||
On June 27, 1988, at 7:59 p.m., the reactor at Big Rock Point achieved | |||
criticality following an 80 day refueling outage. The NRC inspectors | |||
observed the start-up. Besides the normal on-shift crew, an extra Reactor | |||
Operator and Auxiliary Operator were present. The start-up was performed | |||
in a professional manner with detailed procedures. Procedures used during | |||
the start-up were TV-34, "Reactor Start-up with Low Source Counts," | |||
Re<1sion 3, dated February 20, 1987; General Operating Procedure (GOP) 1, | |||
"Plant Start-up from Cold Shutdown," Revision 115, dated May 14, 1988; ' | |||
and Technical Data Book 15.5.I.2, "Control Rod Withdrawal and Insertion | |||
Sequence Cycle 23," Revision 82. | |||
The plant continued to heat up within required limits and the required | |||
turbine overspeed trip tests were performed. Problems were encountered | |||
when the licensee tried to place the generator on line. When an | |||
electrical problem c: curred in the generator excitation and automatic | |||
voltage control, power ascension was halted to perform repairs. After | |||
rep- were completed and power was raised to approximately 20 megawatts | |||
elt ., control room Operators noted that each one of the three | |||
nei . stalled Wide Range Monitor (WRM) nuclear systems was indicating | |||
lev e than expected. Power ascension was halted until a course of action | |||
could be determined by the Plant Review Committee (PRC). Following | |||
several hours of discussion, the PRC decided to allow Instrument and , | |||
Control (I&C) technicians to move the detectors to a higher flux position. ' | |||
At 4:54 a.m., on June 29, power was raised to 35 megawatts electrical and | |||
a heat balance calculation was performed. | |||
i | |||
I&C technicians using the heat balance calculation results attempted to ! | |||
calibrate the WRMi s with no success. The shift supervisor contacted l | |||
appropriate management personnel and a decision was made to shutdown the | |||
reactor. Plant personnel commenced shutdown at 5:25 a.m., per GOP-6, i | |||
"Plant Shutdown to Hot Shutdown," Revision 115. Shutdown was completed ' | |||
at 7:47 a.m., when all rods were fully inserted. | |||
6 ! | |||
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During.the review of this event, the. licensee determined that the' shutdown | |||
met the criteria of Emergency Plan Implementing Procedures (EPIP-1) and at | |||
8:00 a.m., on June 29, a Notification of-Unusual Event was declared. The | |||
NRC, the State.of Michigan, and the Charlevoix County Sheriff's Department | |||
were notified.within ten minutes. The event was terminated at 2:30 p.m., | |||
when the reactor achieved cold shutdown and the above agencies.were | |||
notified of the same. The licensee contacted General Electric, the | |||
equipment vendor, for assistance and subsequent repairs were completed by | |||
the morning of July 1. A reactor start-up was commenced per procedure | |||
but was terminated at 6:44 a.m., when the source range nuclear instruments | |||
failed to properly respond. A PRC meeting was conducted, a course of | |||
action was determined, subsequent repairs were.made, and post maintenance | |||
testing was completed. A reactor start-up commenced, with criticality | |||
being achieved at 5:41 p.m. on July 1. | |||
When attempting to place the turbine generator on line early on July 2, a | |||
problem with the hydrogen seal oil system was discovered which resulted in | |||
a plant shutdown. Repairs were made and the reactor was re-started on | |||
July 7. The NRC inspector monitored the WRM's during power ascension. | |||
Following a heat balance calculation, I&C personnel were unable to | |||
calibrate WRM Channel 2. The channel was placed in the inoperable | |||
condition and power ascension was stopped until repairs could be | |||
accomplished. General Electric was contacted, repair parts for each of | |||
the three WRM channels were obtained and installed, and the WRM's were | |||
calibrated satisfactorily on July 10. Power ascension was resumed with | |||
heat balance calculations and calibrations of instruments being performed | |||
as necessary. | |||
The NRC has been conducting a separate follow-up inspection of the | |||
problems encountered during the~ start-up of the WRM's. . Inspection | |||
Report No. 50-155/88017(DRS) will be completed after review of the | |||
Licensee's Event Report dealing with the same subject. | |||
No violations or deviations were identified in this area. | |||
8. Licensee Action on IE Bulletins | |||
* | |||
The NRC requested that all licensees review NRC Bulletin No. 88-05, | |||
Supplement 1, "Nonconforming Material Supplied By Piping Supplies | |||
Inc. at Folsom, New Jersey and West Jersey Manufacturing Company at | |||
Williamstown, New Jersey." The bulletin included information on | |||
defactive piping materials supplied by Piping Supplies Incorporated | |||
and also by West Jersey Manufacturing Company. The licensee's | |||
4 | |||
investigation of the problem described in the bulletin revealed that | |||
Big Rock Point had never purchased any material from the above | |||
companies. This item will remain open pending written confirmation | |||
from the licensee. | |||
7 | |||
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.. | |||
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NRC Bulletin No. 88-07, "Power Oscillations In Boiling Water Reactors | |||
(BWR)," issued June 15,.1988, required all BWR licensees to thoroughly | |||
brief all licensed reactor operators or shift technical advisors regarding | |||
the March 9, 1988, LaSalle Unit 2 event within 15 days of receipt. The | |||
event involved excessive neutron flux oscillation while the reactor was on | |||
natural circulation. The licensee completed the briefing of required | |||
on-shift individuals within the 15 days. Other' required members of the ~ | |||
licensee staff who were on leave reviewed the material upon their return. | |||
The SRI reviewed the attendance sheet to verify licensee's actions. | |||
Item 1 of Requested Actions for NRC Bulletin No. 88-07 is closed. | |||
No violations or deviations were ident).'ied in this area. | |||
9. Exit Interview | |||
The inspector met with licensee representatives (denoted in Paragraph 1) | |||
~ | |||
throughout the month and at the conclusion of the inspection period and | |||
summarized the scope and findings of the inspection activities. The | |||
licensee acknowledged these findings. The inspector also discussed the | |||
likely informational content of the inspection report with regard to | |||
documents or processes reviewed by the inspector during the inspection. | |||
The licensee did not identify any such documents or processes as | |||
proprietary. | |||
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}} |
Latest revision as of 06:49, 31 May 2022
ML20151T203 | |
Person / Time | |
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Site: | Big Rock Point File:Consumers Energy icon.png |
Issue date: | 08/05/1988 |
From: | Jackiw I NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20151T187 | List: |
References | |
50-155-88-13, IEB-88-005, IEB-88-007, IEB-88-5, IEB-88-7, NUDOCS 8808160287 | |
Download: ML20151T203 (8) | |
See also: IR 05000155/1988013
Text
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U.S. NUCLEAR REGULATORY COMMISSION
<
l
REGION III I
f
hport No. 50-155/88013(DRP)
Docket No. 50-155 License No. DPR-6
Licensee: Consumers Power Company
212 West Michigan Avenue
Jackson, MI 49201
Facility Name: Big Rock Point Nu ear Plant
Inspection At: Charlevoix, MI 49720
Inspection Conducted: June 2 through July 18, 1988 ,
Inspector: E. Plettner 8'd 7N
Uate
Inspector: N. Williamsen .
Date
t
Approved By: 1 N !
ReactorPyojectsSection28 Date
Inspection Summary
Inspection on June 2 through July 18,1988 (Report No. 50-155/88-013(DRP))
Areas Inspected: The inspection was routine, unannounced, and conducted by-
the Senior Resident Inspector and the Resident Inspector. The functional '
areas inspected consisted of the followina areas. Surveillance observation
of the pressure test on the nuclear steam supply system and the reactor
depressurization system. Maintenance observation of work performed on
motor operated isolation valves and the reinstallation of the reactor
depressurization valves. Operational safety verification, radiological
,
practices, and security observations involving day to day plant activities.
Startup/ refuel activities associated with the refuel and startup of the
reactor. NRC Bulletins on defective piping material and pover oscillations
4
ir, boiling water reactors.
Results: The licensee has demonstrated a desire to respond in a timely
manner to issues and concerns presented to them by the NRC. The surveillance,
maintenanca, operational safety, radiological program, and the security
program appeared to ensure public health and safety. Two violations were
,
identified in this report. The violation in the maintenance section
addresses inadequate quality controls and the violation in the operational
safety section addresses the failure to follow procedure when using a copy
-
of a controlled document.
8808160287 880805
gDR ApoCK 05000155 '
- . PNU
. . . . .- _ _ _ . - - _ . - _ _ - . . _ . ._. _ _ _ _ . _ . _ _ _ _ _ _ _ . _
.
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.
.
.
.
DETAILS
1. Persons Contacted
- T. Elward, Plant Superintendent
- A. Pet'tjean, Planni:ig and Administrative Services
Superintendent
G. Withrow, Engineering Maintenance Superintendent
- R. Alexander Technical Engineer
L. Monshor, Quality As:urance Superintendent
- J. Seer, Chemistry / Health Physics Superintendent
- R. Scheels, ' Acting Operations Supervisor
"R. Hill, Sr. QA Consultant
- P. Donnelly, Nuclear Assurance Administrator
- R. Schrader, E & M Superintendent, Acting .
- M. Bielinski, Production and Plant Performance,
Superintendent, Acting
- T. Hagan, Director Nuclear Training
The inspector a'.so contacted other licensee personnel in the Operations,
Maintenance, Radiation Protection, and Technical Departments.
- Denotes those present at exit interview.
2. Monthly Surveillance Observation (61726)
The NRC inspectors observed Technical Specification required surveillance
tests. The reviews and observations were conducted to verify that facility
surveillance operations were performed in accordance with the requirements
established in the Operating License and Technical Specification.
The Senior Resident Inspector (SRI) observed the licensee's performance
of the following surveillance tests on the indicated dates:
June 20, 1988, TV-10, "Pressure Test of Nuclear Steam Supply System,"
Revision 37, dated June 14, 1988, with approved. temporary changes to
allow the use of a new hydro test pump. A failed relief valve in the
Reactor Water Clean-up System was noted during the test. A maintenance
work order was issued and a new valve installed. The licensee also
replaced two other relief valves in the system since they were the same
age as the failed valve. A second test was performed and observed by
the SRI on June 22, 1988, with satisfactory results.
July 13,1988, T30-30, "RDS Cabinet Test (Sensor Cabinet C/ Actuation
Cabinet 3)," Revision 24, dated January 11, 1988. The procedure was
satisfactorily performed by a licensed operator and an auxiliary
operator.
No violations or deviations were identified in this area.
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3. Monthly Maintenance Observation ' ?703)
Station maintenance activities of safety related systems and components
listed below were observed / reviewed to ascertain that they were conducted
in accordance with approved procedures, regulatory guides and industry
codes or standards and in conformance with technical specifications.
The following items were considered during this review: the limiting .
conditions for operation were met while components or systems were removed
from service; approvals were obtained prior to initiating the work;
activities were accomplished using approved procedures and were inspected
as applicable; functional testing ond/or calibrations were performed prior
to returning components or systems to service; quality control records
were maintained; activities were accomplished by qual fied personnel;
parts and materials used were properly certified; radiological controls
were implemented; and fire prevention controls were implemented.
Work requests were reviewed to determine status of outstanding jobs and to
assure that priority is assigned to safety-related equipment maintenance
which may affect system performance.
On June 18, 1988, the SRI observed the performance of maintenance on
motor operated Valve IA-760 under Work Request 88-PCS-0075.
The SRI reviewed the certification test reports of the Reactor
Depressurization System Valves from Wyle Laboratory. The certification
reports identified each main valve and its associated pilot valve, the
full-stroke time, the leak rates, acceptance criteria, and test proceoure
used to perform the test. Pilot valve assembly number one failed the test
on the first attempt. Repairs were made and testing was conducted with
the second test results being satisfactory. The certificate numbers were
49294-1, -2, -3, and -4. The SRI observed the installation of the valves
on June 24 and 25, 1988, under Maintenance Work Orders 88-RDS-065 and 066.
During the refueling / maintenance outage the licensee replaced the
diaphragms in the Control Rod Drive Scram Valves (CRDSV), a safety-related
system. All 64 valve diaphragms were replaced and tested for proper
operation. It was during post maintenance testing that personnel
discovered excessive air leakage from the valves. The licensee
investigated the problem and found that the diaphragms had been installed
upside down and, in addition, four of the 64 diaphragms had been
incorrectly manufactured resulting in failure of the diaphragms.
Subsequently, all 64 diaphragms, manufactured by Hammel-Dahl, were replaced
for a second time. The licensee sent a letter to General Electric and the
Boiling Water Reactor Owner's Group to inform them of the possible
defective diaphragms. Big Rock Point was one of the first plants to
replace these diaphragms because of General Electric's Service Information
Letter No. 457. The SRI inquired into the amount of Quality Control (QC)
provided during the maintenance activity. The results of the inquiry
revealed that QC had reviewed the purchase agreement documents before work
and work completion documents. During the first installation performed in
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April and May.1988, of the 64 diaphragms, no member'of:the plant's QC
organization observed the activity through one complete disassembly,
repai*, and reassembly process. No inspection was performed to include a
dimensional. check of the diaphragms or a comparison between diaphragms fcr
consistency. The failure to inspect installation activities.and perform
measurements or tests of material ~ is an apparent violation of quality .
control requirements of 10 CFR 50, . Appendix B, Criterion X, as implemented
by Big Rock Point's, "Quality Assurance Description for Operational Nuclear
Power Plants," as described in Section 10. (155/88013-01).
Work on the CRDSVs was performed by Consumers Power Company's traveling ,
maintenance crew who had their own supervisor. Training was conducted
for the crew prior to allowing work to commence on the CRDSV. Corrective
actions taken b/ the licensee prior to the second installation in June
1988, were to revise the installation procedure, and have a plant QC
individual observe at least one complete installation, The SRI verified
by record review and interview that the licensee implemented the
corrective actions. Full-stroke testing proved operability of the CRDSV.
This problem resulted in an extended outage, a great deal of rework and
testing, and additional cost to purchase the replacement parts.
One violation was identified in this area.
4. Operational Safety Verification (71707)
The inspector observed control room operations, reviewed applicable
logs, and conducted discussions with control room operators-during the
inspection period. The inspector verified the operability of selected
emergency systems, reviewed tagout records, and verified proper return
to service of affected components. Tours of the containment sphere and
turbine building were conducted to observe plant equipment conditions,
including potential fire hazards, fluid leaks, and excessive vibrations
and to verify that maintenance requests had been initiated for equipment
in need of maintenance. The inspector observed plant housekeeping /
cleanliness conditions and controls. During the. inspection period,
the inspector walked down the accessible portions of the Reactor.
Depressurization Post Incident, Core Spray, and Containment Spray
systems to. verify operability.
During plant tours conducted this period, the SRI noted that. copies of the
controlled documents used to direct safety activities listed below were
found at their associated work site without being marked "Working Copy"
or "Working Controlled Copy," on the date shown:
June 18, 1988: System Operating Procedures (S0P) 19, "Make up
System," Revision 140.
June 21, 1988: S0P 15, "Condensate System," Revision 94.
June 21, 1988: 50P 11, "Radioactive Waste System," Revision 117.
July 6, 1988: Administrative Procedure 4.2.1, "Material
Control," Revision 4.
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10 CFR 50, Appendix B, Criterion V, as implemented by Big Rock Point's,
"Quality Assurance Program Description for Operational Nucle'ar Power
Plants," as described in Section 5.0, requires that activities affecting
quality shall be prescribed by documented procedures. Administrative
Procedure 4.1.8 "Procedure Assurance," Revision 1, dated February 12, 1988,
Section 12.0 titled "Short Term Controlled Documents," requires that
controlled documents needed as working level procedures shall be clearly
marked "Working Copy" or "Working Controlled Copy." Failure of the three
working SOP's and the working Administrative Procedure to be marked
"Working Cr,sy" or "Working Controlled Copy," is an apparent violation.
(155/88013-02).
One violation was identified in this area.
5. Radiological Protection Observations (71709)
The NRC inspectors verified that-selected activities of the licensee's -
radiological protection program were. implemented in compliance with
the facility policies, procedures, and regulatory requirements. The
activities observed and/or reviewed during this inspection period were
that health physics (HP) supervisory personnel were conducting plant tours
to check on activities in progress. Radiation work permits contained the
appropriate information to ensure work was performed in a safe and
controlled manner. Personnel in radiation controlled areas (RCA) were
wearing the required personnel monitoring equipment and protective
clothing. Radiation and/or contamir.sted areas were properly posted and
controlled based on the activity levels within the area. Personnel
properly frisked prior to exiting an RCA.
No violations or deviations were identified in this area.
6. Security Observations (71881)
The NRC Inspectors verified by observation or record review that physical
security measures were being implemented as prescribed in the licensee's
approved physical security plan. The elements contained in the inspection ,
were security manning requirements, access control of both personnel and' !
vehicles, and detection / assessment aids. Throughout the inspection
period, the inspectors observed that personnel within the protected area )
(PA) properly displayed their identification badges. Vehicles were '
properly authorized, searcheu, and escorted or controlled within the PA.
Persons and packages were properly checked and cleared before entry into
the PA. When security equipment failure or impairment occurred the 1
required compensatory measures were empluyed. Security force actions !
were conducted in a professional manner. '
No violations or deviations were identified in this area.
7. Startup Testing - Refueling (72700)
On June 11, 1988, during refueling operations the licensee found that a l
fuel bundle could not be placed into the position required by the fuel !
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load sequence Procedure TR-46. . Fuel loading activities were stopped until
the problem could be resolved. The reactor had been verified subcritical
throughout the performance of the procedure. Core verification was
performed with a TV camera to ensure all remaining fuel bundles were
correctly loaded. No other bundles were found out of position. The
reactor engineer made the necessary temporary changes, with approval, to
the fuel load sequence procedure to place the misplaced bundle into.its
correct position. The remaining steps of the procedure were completed
without further problems. Final core verification was performed
satisfactorily. The. licensee will be performing an' evaluation to
determine the root cause and recommend actions to prevent reoccurrence.
This apparent violation of the fuel load sequence procedure will not be
issued because it appears to meet the five criteria stated in 10 CFR 2,
Appendix C (V), Section G.1: (a) it was identified by the licensee;
(b) it fits in Severity Level IV or V; (c) it was reported, if required;
(d) It is being corrected including measures to prevent recurrence, within
a reasonable time; and (e) it was not a violation that could reasonably be
expected to have been prevented by the licensee's corrective action for a
previous violation.
On June 27, 1988, at 7:59 p.m., the reactor at Big Rock Point achieved
criticality following an 80 day refueling outage. The NRC inspectors
observed the start-up. Besides the normal on-shift crew, an extra Reactor
Operator and Auxiliary Operator were present. The start-up was performed
in a professional manner with detailed procedures. Procedures used during
the start-up were TV-34, "Reactor Start-up with Low Source Counts,"
Re<1sion 3, dated February 20, 1987; General Operating Procedure (GOP) 1,
"Plant Start-up from Cold Shutdown," Revision 115, dated May 14, 1988; '
and Technical Data Book 15.5.I.2, "Control Rod Withdrawal and Insertion
Sequence Cycle 23," Revision 82.
The plant continued to heat up within required limits and the required
turbine overspeed trip tests were performed. Problems were encountered
when the licensee tried to place the generator on line. When an
electrical problem c: curred in the generator excitation and automatic
voltage control, power ascension was halted to perform repairs. After
rep- were completed and power was raised to approximately 20 megawatts
elt ., control room Operators noted that each one of the three
nei . stalled Wide Range Monitor (WRM) nuclear systems was indicating
lev e than expected. Power ascension was halted until a course of action
could be determined by the Plant Review Committee (PRC). Following
several hours of discussion, the PRC decided to allow Instrument and ,
Control (I&C) technicians to move the detectors to a higher flux position. '
At 4:54 a.m., on June 29, power was raised to 35 megawatts electrical and
a heat balance calculation was performed.
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I&C technicians using the heat balance calculation results attempted to !
calibrate the WRMi s with no success. The shift supervisor contacted l
appropriate management personnel and a decision was made to shutdown the
reactor. Plant personnel commenced shutdown at 5:25 a.m., per GOP-6, i
"Plant Shutdown to Hot Shutdown," Revision 115. Shutdown was completed '
at 7:47 a.m., when all rods were fully inserted.
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During.the review of this event, the. licensee determined that the' shutdown
met the criteria of Emergency Plan Implementing Procedures (EPIP-1) and at
8:00 a.m., on June 29, a Notification of-Unusual Event was declared. The
NRC, the State.of Michigan, and the Charlevoix County Sheriff's Department
were notified.within ten minutes. The event was terminated at 2:30 p.m.,
when the reactor achieved cold shutdown and the above agencies.were
notified of the same. The licensee contacted General Electric, the
equipment vendor, for assistance and subsequent repairs were completed by
the morning of July 1. A reactor start-up was commenced per procedure
but was terminated at 6:44 a.m., when the source range nuclear instruments
failed to properly respond. A PRC meeting was conducted, a course of
action was determined, subsequent repairs were.made, and post maintenance
testing was completed. A reactor start-up commenced, with criticality
being achieved at 5:41 p.m. on July 1.
When attempting to place the turbine generator on line early on July 2, a
problem with the hydrogen seal oil system was discovered which resulted in
a plant shutdown. Repairs were made and the reactor was re-started on
July 7. The NRC inspector monitored the WRM's during power ascension.
Following a heat balance calculation, I&C personnel were unable to
calibrate WRM Channel 2. The channel was placed in the inoperable
condition and power ascension was stopped until repairs could be
accomplished. General Electric was contacted, repair parts for each of
the three WRM channels were obtained and installed, and the WRM's were
calibrated satisfactorily on July 10. Power ascension was resumed with
heat balance calculations and calibrations of instruments being performed
as necessary.
The NRC has been conducting a separate follow-up inspection of the
problems encountered during the~ start-up of the WRM's. . Inspection
Report No. 50-155/88017(DRS) will be completed after review of the
Licensee's Event Report dealing with the same subject.
No violations or deviations were identified in this area.
8. Licensee Action on IE Bulletins
The NRC requested that all licensees review NRC Bulletin No. 88-05,
Supplement 1, "Nonconforming Material Supplied By Piping Supplies
Inc. at Folsom, New Jersey and West Jersey Manufacturing Company at
Williamstown, New Jersey." The bulletin included information on
defactive piping materials supplied by Piping Supplies Incorporated
and also by West Jersey Manufacturing Company. The licensee's
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investigation of the problem described in the bulletin revealed that
Big Rock Point had never purchased any material from the above
companies. This item will remain open pending written confirmation
from the licensee.
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NRC Bulletin No. 88-07, "Power Oscillations In Boiling Water Reactors
(BWR)," issued June 15,.1988, required all BWR licensees to thoroughly
brief all licensed reactor operators or shift technical advisors regarding
the March 9, 1988, LaSalle Unit 2 event within 15 days of receipt. The
event involved excessive neutron flux oscillation while the reactor was on
natural circulation. The licensee completed the briefing of required
on-shift individuals within the 15 days. Other' required members of the ~
licensee staff who were on leave reviewed the material upon their return.
The SRI reviewed the attendance sheet to verify licensee's actions.
Item 1 of Requested Actions for NRC Bulletin No. 88-07 is closed.
No violations or deviations were ident).'ied in this area.
9. Exit Interview
The inspector met with licensee representatives (denoted in Paragraph 1)
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throughout the month and at the conclusion of the inspection period and
summarized the scope and findings of the inspection activities. The
licensee acknowledged these findings. The inspector also discussed the
likely informational content of the inspection report with regard to
documents or processes reviewed by the inspector during the inspection.
The licensee did not identify any such documents or processes as
proprietary.
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