ML20203A014

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Insp Rept 50-155/97-15 on 971205-980202.Violations Noted. Major Areas Inspected:Facility Management & Control, Decommissioning Support Activities,Spent Fuel Safety & Radiological Safety
ML20203A014
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 02/14/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20202J818 List:
References
50-155-97-15, NUDOCS 9802230240
Download: ML20203A014 (24)


See also: IR 05000155/1997015

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U.S. NUCLEAR REGULATORY COMMIS810N

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REGION lil

! Docket No: 50 155

License No: DPR 06

Report No: 50155/97015(DNMS)

Licensee: Consumers Energy Company

Facility: Big Rock Point Nuclear Power Plant

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Location: 10269 U.S. 31 North

t Charlevoix, MI 49720

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Dates: December 5,1997 February 2,1998

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Inspectors: R. J. Leomon, Senior Resident inspector

C. E. Brown, Resident inspector -

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R. B. Landsman, Project Engineer

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J. E. House, Senior Radiation Specialist

P. W. Harris, License Project Manager

Approved by: Bruce L Jorgensen, Chief

Decommissioning Branch

Division of Nuclear Materials Safety

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9802230240 980214

PDR ADOCK 05000155

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EXECUTIVE SUMMARY

Big Rock Nuclear Power Plant

NRC Inspection Report 50155/97015

This routine decommissioning inspection covered aspects of facility management and control,

decommissioning support activities, spent fuel safety, and radiological safety.

-e Overall, the licensee's performance during the chemical decontamination process was

good. However, there were two instances of poor performance in the health physics

area.

Facility Manno 9 ment and Control

e The inspector concluded that changing the Site Emergency Plan to reduce the minimum

shift crew composition by one control room operator and one auxiliary operator was within

the current TS requirement for a plant in cold shutdown.

  • Good cooperation and teamwork between the contractor and plant staN resulted in a high

quality, workable procedure to be used in the chemical decontamination process,

o Overell, the chemical decontamination of the primary system was a success. Reduced

dose rates should enable workers to dismantle the plan' faster witn lower accumulated

radiation doses, and with less risk of altbome contamination when major

piping / equipment systems are breached.

  • The plant safety review committee evaluated twenty plant systems classified as non-Q -

and determined they are not needed for a pemianently defueled plant. These systems

were designated as available for decommission!ng,

o Administrative Procedure D1.11 " Safety Evaluation," was revised such that the

requirements of 10 CFR 50.82 were incorporated into the procedure. The licensee's use

of Procedure D1.11 should help ensure that the decommissioning fund will always

contain enough money to go to SAFESTOR or to complete the total decommissioning

job.

Qt&gmmiulonino Support ActlMel

e Installation of a HEPA filter in the reactor building ventilation was completed in December

1997, completing a PSDAR commitment and bringing the ventilation system in

compliance with the FGEIS. The ventilation system now has filtration for containment

exhaust air.

e The time for the SFP to heat-up from 80' F to 150' F was verified by actual testing to be

greater than the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> assumed in the licensee's submittal to the NRC.

  • The materialintegrity of structures, systems, and components necessary for safe

storage of spent fuel and conduct of safe decommissioning was being maintained, and

plant housekeeping and fire protection wem generally good.

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Spent Fuel Safety

e The inspector concluded that the licensee can readily accommodate various conditions

that may challenge integrity of the fuel.

  • A concern was identified relating to the potential for an individual inadvertently pulling up

a high dose item suspended on a cable in the SFP high exposure. Plant management

had the SFP covers put on the pool as a temporary solution.

RadiologiseL6.aMy

  • The inspectors identified one violation of Technical Specifications conceming a

decontamination worker in a HRA not monitoring his dosimetry as required and not noting

that his ELD was on pausr. This inciden' indicated that worker attention to radiation

protection practices (especially in the area of monitoring dosimetry), remained a problem

for the station personnel.

  • The chem decor project included appropriate dose minimization planning, and effectively

incorporated ALARA principles.

  • The licensee's radiation prctection program for the chem decon prncess was also well

executed. Communication between licensee personnel and the vendor performing the

chem decon were very good.

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Egoori Detalls

EVinalgrYJofEant Activitin

The reactor coolant, shutdown cooling, and cleanup systems were chemically decontaminated.

Licensed reactor and senior reactor operators completed requalification training to keep their

NRC licenses active. Tests on spent fuel pool (SFP) heatup rates were conducted, twenty-plant

systems were classified as available for decommissioning, and the emergency plan exercise was

deferred until March 1998.

1. Facility Management and Control

1.1 Genersj

The in,spectors conducted frequent reviews of ongoing plant activities and attended

licenten meetings and reviews addressing these activities, in order to assess overall

facility management and controls. Specific events and findings are detailed in the

sections below,

l.2 QID#alleligBlaQRS9 ment. aniCMLQontrols at Permanently Shyt Down RfAcigIn

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l.2.1 QantIgj

The inspectors reviewed the licensee's systems for overall management and control of

the decommissioning process. Specific processes which were selectively examined

included the programs for identification and resolution of safety concems and the

commitment tracking programs and procedures. The inspectors also reviewed and

evaluated the licensee's organization, staffing, qualifications and training, including those

for the contracted workforce, to verify that licensing commitments were being met.

Reference was made to the requirements detailed in the technical specifications (TS),

and the post shutdown decommisaloning activities report (PSDAR). The inspectors also

selectively examined and evaluated the licensee's planning and scheduling to determine

their effectiveness. The effectiveness of the licensee's review of regulatory information.

Including information notices applicable to the facility, was selectively examined. Specific

events and findings are detailed in the section below.

l.2.2 Sigtfina and_ Qu_a_liftcations

a. S_qpng

The inspecter reviewed the process for licensed reactor and senior reactor operators

maintaining license qualifications, and for qualifying operators as certified fuel handlers,

b. Observations and Findinas

On December 16,1997, licensed reactor and senior reactor operators completed

requalification training and passed required testing to meet NRC license requirements;

thus, maintaining their NRC licenses. Ir. January 1998, the licensee started certified fuel

handling training, which takes about seven weeks to complete.

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c. Qpnclusion

The licensee was effectively completing operstor license qualificatione and certified fuel

handlers' training.

1.2.3 EnitIgencyflan_SteILend_Schedvit

a. Ssopp

The inspector followed developments relating to emergency plan exercise rescheduling,

and attended a Plant Review Committee (PRC) meeting where changes to the Site

Emergency Plan, Volume 9, Chapter 5 Section 1.1.1, * Normal Organization" were

discussed. The inspector observed discussion of the changes and the safety evaluation,

b. Observations and Findinas

After discussions with the NRC, the State of Michigan, and FEMA, on December 30,

1997, the licensee was granted a scheduler exemption to defer the 1997 emergency

exercise until March 1998. The new emergency preparedness scenario will represent the

permanently defueled plant.

On January 27,1998, the PRC discussed changes to the Site Emergency Plan that would

change the normal organization (shift complement) from one shift supervisor (SS), two

control room operators, and two auxiliary operators, down to a shift complement of one

SS, one control room operator, and one auxillary operator.

The inspector verified TS 6.2.2, Table 6.21, ' Minimum Shift Crew Composition for a

Shutdown or Cold Shutdown Plant," which requires one SS, one control room operator,

and one auxiliary operator.

The PRC concluded that this change in staffing level would not result in an unreviewed

safety question (USQ), and the change is planned for March 1998,

c. CgaplV1100

Changes to the Site Emergency Plan to reduce the minimum shift crew composition by

one control room operator and one auxillary operator were within the current TS

requirements for a plant in cold shutdown.

l.3 ELalcly31ylewAJfal0D_ChBBatkapdfdOAlfications at Permamently Shut Down ReactoIs

(37801)

1.3.1 Chemical Decontamination Procedure

a. Scope

in December 1997, during PRC meetings, the inspector observed the safety review

process applied in discussions and interaction between licensee and contractor personnel

when Procedure O PCS 01," Primary Coolant System Operations During Chemical

Decontamination," was developed and approved.

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b. Observations and Findinns

The inspector verified that a quorum was present and evaluated ongoing discussion for

the determination that the proposed procedure or changes to the procedure were not

USQs The inspector reviewed the completed procedure prior to the start of the chemical

decor.tamination process.

Items that could possibly be a safety concem were well discussed and resolved by

making procedure changes. The changed procedure' , as retumed to another PRC for

further discussion before determining that a USQ did not exist.

c. Conc!unlen

Good cooperation and teamwork between licensee and contractor personnel resulted in a

high quality, workable procedure to be used in the chemical decontamination process.

l.3.2 Chemical Decontaminatl2D

a. Scope

The inspector examined an extensive chemical decontamination (chem decon) which the

licensee performed on the reactor vessel, steam drum, coolant pumps, primary piping,

and portions of the reactor water cleanup system heat exchangers. The purpose of the

chem decon was to remove contamination from the inside surfaces of reactor system

components in order to accomplish a major reduction in dose rates in the vicinity of those

components through which reactor coolant flowed. The process was designed to provide

a cost effective way to reduce radiation exposure and to concentrate radweste for

disposal, thus reducing radwaste disposal costs,

b. Qb.tifythons and Findinas

The overall process proceeded smoothly with few problems. Over 400 curies of

radioactive material were removed from system components and dose rates were

reduced by a factor or 10 or greater. Isotopic activity and curie removal were estimated

by gamma spectroscopy.

The licensee's quality assurance program for the gamma spectroscopy instrumentation

was adequate. A review of instrument control charts indicated that the detector systems

were operating under statistical control.

As this was the first time that this process had been used on an intact plant, there was

minimal industry experience available to assist the licensee in job planning and execution.

From reviewing the work schedule and the results of the overall chem decon process, it

was evident that licensee and vendor planning were thorough and that licensee vendor

communications were very effective. There was minimal schedule slippage, and the

transition from system heat up to chemical injection appeared to have been relatively

trouble free. During the process the licensee identified two system leaks which were

isolated and contained.

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c. Conclusion

Reduced dose rates should enable workers to dismantle the plant faster with lower

accumulated radiation doses. There should also be fewer opportunities for airbome

contamination when major pipinglequipment systems are breached since most

contamination has been removed from interior surfaces of components,

l.4 D9_ggmmill10DlDafttformance_and Stalys Review at Permanentiv_ Shut Down ReggigIs

(71801)

1.4.1 Challenoes burino the Chemical Decontamination Process

a. Scone

The inspector observed activities related to the chemical decontamination process and

noted what challenges arose and how they were addressed.

b. Observations _end Findinas

The challenges and actions to successfully complete the chemical decontamination

process were as listed below:

Items during system setup and startup:

  • An air valve, connected to the reactor head during the system setup, leaked

through an open ended pipe. A small quantity of radioactive water spilled into the

containment when the reactor water level was raised. A blank flange was

installed on the pipe and the water level was lowered to stop the leak. - The leaky

valve was then replaced.

e The licensee moved up the scheduled flow test of main flow pump P 12 and

performed the test without lead shielding blankets around the filter housing.

During the flow test, a crud burst occurred which the licensee did not anticipate.

The crud apparently collected in the filter while the system was idle for several

months. The local area dose rate increased from that of a radiation area to a rate

meeting the requirements for a high radiation area. The containment was

evacuated by the health physics (HP) technicians until the dose in the area was

understood,

e The crud burst during the pump startup put crud into piping dead legs, causing

hot spots.

  • A contractor was using duct tape to label the valves on the control panel for the

air operated valves. Some of the tape was coming off of the control panel. The

inspector considered using duct tape for labeling a poor practice After the

inspector raised this concem, the duct tape was replaced with permanent marker

labels.

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Items during operation of the system:

e Operations did not identify that a bypass line in the non regenerative heat

exchanger that contained a sample valve with a leaky, carbon steel threaded

reducer. Carbon steel was strongly attacked by the hot flush chemical which

flowed through the threaded leak path and ate away the reducer threads. This

caused a breach in the piping and a 7 spm leak of reactor coolant. The chemical

decontamination process was shut down for several hours, until the leaking valve

was found and closed.

  • Main flow pump P 12 sealleakage increased and the pump had to be replaced

with the spore pump. This was a planned contingency.

  • More resins were used than expected and more had to be ordered. More room

had to be made in the waste disposal system for the storage of the extra used

resin.

e The emergency diesel generator (EDG), which powered the P 12 pump, ran

continuously for several days. The EDG developed both a lubricating oilleak and

a fuel oil leak, and the turbo charger was alsn using oil. After seven days of

continuous running, the EDG was shut down and the attemate EDG was wired in

and run. The oilleaks were repaired and the turbo-charger was replaced. The

EDG was then retumed to powering the P 12 pump. Use of the attemate EDG

was a planned contingency.

The inspector observed the following strengths during the chemical decontamination

process:

  • Contract management worked well with licensee management and a Good flow of

communication was evident. The shift supervisor and control room were also

kept informed of all activities that contractors were performing.

  • The original estimate was that the chemical decontamination process would

remove 300 curies of activity. The chemical decontamination process removed

400 curies during the het flush and about 8 curies during the cold flush. The

filters also removed 12 curies of activity.

  • Overall, the decontamination factor was at least 10 inside the piping, which was

the objective of the decommissioning process,

c. Conclusion

This was the first time that this chemical decontamination process was used in the field at

a nuclear power plant. The number of curies of activity removed from the piping was

about 100 curies more than expected. However, this extra activity used more resins than

expected and the radwaste problem associated with the extra resin had to be dealt with.

The inspector identified several challenges and some strengths during this chemical

decontamination process. Overall, the chemical decontamination was a success.

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1.5 Plant Procedures M2700)

1.5.1 Systems Available for becommissionina

a. Scope

The inspector reviewed the licensee's process for safely determining that a plant system

was no longer needed to support the safe operation of the spent fuel pool or the spent

fuel pool cooling system. The inspector also attended a Plant Safety Review Committee

(PRC) meeting where changes to the Quality List, Chapter 6, " Classification of Systems'

were reviewed. This screening process reclassified systems as Non-Q for a permanently

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defueled plant and therefore available for decommissioning.

b. Observations and Findinat

on January 28,1998, the inspector observed members of the PRC meeting concoming

the classifications of systems and the determination that systems were no longer needed

for a permanently defueled plant. The list of syt ns determined to be available for

decommissioning was as follows:

. Air Ejectors and Mechanical Vacuum Pump

.- Altemate Shutdown System

. Containment Gamma Mcnitoring System

. Control Rod Drive System

. Emergency Condenser System

. Feedwater System

. Extraction Water Drains

. Liquid Poison System

. Main Steam System

. Neutron Monitoring System

. Primary Coolant System

. Post incident System

. Reactor Cleanup System

. Reactor Depressurizing System

. Reactor Protection System

. Reactor Steam Drum

. Reactor Vessel, General

. Reactor VesselIntemals

. Turbine Generator System

. Off Gas System

c. Conclusion

The PRC determined that twenty plant systems are classified as non-Q and are not

needed for a permanently defueled plant. They also determined that these systems are

available for decommissioning. The inspector did not have any concerns with the PRC's

determination that these systems are not needed for the safe operation of the spent fuel

pool or spent fuel pool cooling system.

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1.5.2 Screening Requirements of 10 CFR 50.82 Added to Safety Evaluation Pmeedure

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The inspot x reviewed 10 CFR 60.82 ' Termination of Lloonse,' and Administrative l

Procedure D1.11, ' Safety Evaluations,' to determine that Procedure D1.11 contained i

applicable requirements of 10 CFR 50.82.  !

b. . Observations and Findings  ;

The plant safety evaluation Procedure D1.1i, Revision 0, was revised to incorporate 10 i

CFR 60.82 screening requirements. Future plant conf 6guration changes will require - l

reviews against the artierta of 10 CFR 60.69.6c and 59.82. The procedure revision

incorporates the three fundamental screening requirements of 60.82 as follows: licensees

- shall not perform any decommissioning activities that 1) foreclose release of the site for

possible unrestricted use; 2) resuN in significant environmental impacts not previously

reviewed; or 3) resuN in there no longer being reasonable assurance that adequate funds

will be available for decommissioning.

c. Conclusion

The applicable requirements of 10 CFR 60.82 were incorporated into Procedure D1.11 I

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  • Safety Evaluation". The licensee's use of Procedure D1.11 should help ensure that '

enough money to go to SAFESTOR or to complete the total decommissioning job will

always be available, l

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1.6 Onsite Follow-uo. Written Reoorts of Non-routine Events at Power Reactor Facilities

(92700)

1.6.1 (Open) VIO 50165/96002-07: Failum to ensure combustible resterials are controlled _

according to T8. The inspector reviewed the proposed corrective actions for this - l

l violation, which relate mainly to outage work. There was no refueling outage in 1997.  ;

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. The licensee will be performing similar dismantlement activities within the next few

[ months. The inspector will then determine if the corrocove actions were effective. This ,

4 item remains open. {

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o ~ 1.6.2 _ (Closed) IFl 50155/96006-03: - Sufficient core spray flow. The post incident system relief )

valves were set at 155 psig and would lift each time the diesel fire pump ran An ,

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engineering evaluation was performed, and the relief valve portion of the system was

L upgraded from 150 psig to 200 psig and the relief valves were replaced with 200 psig '

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valves. The licensee performed a safety evaluation which determined that the system is

!.- not required for plant safety in a permanently defueled plant. This inspector follow-up

i- _ ltem is closed.

l.6.3 (Closed) IFl 50155/96007-02: Delayed dispatch of operational suppori center (OSC)

emergency response team during the 1996 emergency exercise. The OSC response

. team will no longer be exercised due to the plant being permanently defueled. - Therefore, ,

'" this item is no longer relevant and is closed.

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II. Decommissioning Support Activities

11. 1 M8101tampe and Sp.tyMlance_ALPJtmlanently Ghutdown. Reactors (02tu)1)

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II.1.1 Qgnetsj

The inspection evaluated maintenance and surveillance for structures, systems, and

components (SSCs) potentially affecting the safe storage of spent fuel and reliable

operation of radiation monitoring and effluent control equipment. Direct observations,

reviews, and interviews of licensee personnel were conducted to assess whether

maintenance and surveillance were performed in accordance with regulatory

requirements and resulted in the safe storage of spent fuel and reliable operation of

radiation monitoring and efnuent control equipment. This included the proper

implementation of TS and 10 CFR 50, Appendix B, requirements. An examination of

planned or completed maintenance and surveillance activities was conducted to assess

the maintenance and surveillance process from its inception to its completion.

11. 1 . 2 Installrdon and Testina of Hiah Efficiency Particulate Air (HEPA) Filters

a. tigg.g

The inspector reviewed the PSDAR, work packages, and safety evaluation; held

discussions with the project engineer; and walked down the filter system related to the

installation and testing of the HEPA filters,

b. Observations and Findinas

The Big Rock Point Plant's original design lacked HEPA filters in the reactor building

exhaust. In December 1997, the plant installed HEPA filters for use in the unlikely event

of potential accidents. This installation of HEPA filters brings the plant fully within the

bounds of the requirements of the Final Generic Environment impact Statement (FGEIS).

The HEPA filters were installed prior to the performance of the primary system chemical

decontamination. When the efficiency of the filters was tested, the results were not as

designed. The design efficiency was 99.95 percent efficient and the final test efficiency

was 99.70 percent efficient. The licensee performed an engineering analysis that

accepted the test results as adequate for the performance of the chemical

decontamination. The licensee plans to repair the bypass flow in the filter housing to

bring the filter efficiency up to the design value,

During startup testing of the dampers and the filter flow path, on two occasions the

damper repositioned. One situation was resolved by placing a lock washer under the

wing nut to hold the damper in positon. The operating crew Wa' '.hecking th' "ghtness

of the wing nut twice per shift in accordance with a January 30,1o98, de M *. The

other preblem was corrected by putting a tack weld on the "U" clamps ars .,tp i damper

shaft to the damper plate to keep the plate from rotating on the damper shaft. i his work

was accomplished by work order VAS-12711277.

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One flow problem remained unresolved. Flow induced vibrations on damper VHV324 will

require an up stream flow straightener to be installed to correct the vibration situation.

This is an inspector follow-up item (50-155/97015 01(DNMS)).

c. Conclusion

Installation of a HEPA filter in the reactor building ventilation was completed in December

1997, satisfying a PSDAR commitment and bringing the ventilation system up to

compliance with the FGEIS. The ventilation system now has filtration for containment

exhaust air.

11. 1 . 3 SpanLEnel Pool HagippRgle

a. Hopp3

The inspector reviewed the results of TV 59,' Fuel Pool Heatup Tests," to assess

whether decay heat in the pool has declined at the expected rate,

b. Obscrvations and Findinas

On January 28,1998, TV 59, * Fuel Pool Heatup Tests," was performed. Flow was

stopped for 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br />, and the SFP heated up from 50' F to 60' F; this is a heatup rate of

0.526' F/hr. The calculated time for the SFP to heat from 80' F to 150' F was 133

hours. The time to heat up from 50' F to 150' F was calculated as 190 hours0.0022 days <br />0.0528 hours <br />3.141534e-4 weeks <br />7.2295e-5 months <br />. The SFP

is currently averaging 50' F.

The importance of the length of time for the spent fuel pool (SFP) to heat up to 150' is to

have significant time for the licensee to restore SFP cooling if SFP cooling is lost. The

licensee is committed to restore SFP cooling before SFP temperature exceeds 150'so

that the concrete structure of the SFP does not degrade.

The results of TV 59 to date are as follows:

  • November 22,1997 0 60' F/hr
  • December 20,1997 0.b6' F/hr
  • January 28,1998 0.53' F/hr

c, Concj9319D

The time for the SFP to heat up from 80' F to 150' F was verified by actual testing to be

more than the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> assumed in the licensee's submittal to the NRC.

11. 1 . 4 Steam Drum level Indication in the Control Reg

a. S.9222

The inspector observed that the steam drum levelindication in the control room was not

functioning, raising a concern that the control room operators didn't have adequate level

indication to monitor for leaks from the reactor coolant system.

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b. Observations and Findinas

On January 27,1998, the steam drum level Indication in the control room was not

working. The level reference legs had not been refilled after chemical decontamination

flushes and there was a slow leak from the reference leg. The chart recorder level had

been drifting up as the levelin the steam drum had been slowly dropping because the

reference leg was draining. Over a 4 day week end, the operators were without control

room steam drurr,levelindication. The reactor was empty of fuel, but the steam drum

was full of radioactive water. The operators had no chart trend indication or permanent

chart recording of the reactor coolant system level. However, operators were logging a

local pressure and RCS pressure as attemate level monitoring indications. The inspector

discussed this situation with the SS, maintenance manager, acting operations manager,

and the plant manager was assured that the control room steam drum level would be

restored.

On January 28,1998, the steam drum levellndication was filled and vented, and drum

level indication was restored in the control room. Steam drum level was again being

recorded on the level recorder. A daily order was written to communicate to all crews

how to maintain steam drum level and where to maintain the level.

c. Conclusion

The operating management became lax in maintaining steam drum level indication in the

control room after the reactor was defueled. After the inspector held discussions with

plant management, the steam drum levelindication was restored to service. The

operations and maintenance staffs may tend to neglect potentially important

instrumentation once TS no longer require its operation.

11. 2 Operational Safety Verification (71707)

11.2.1 General

The inspectors conducted frequent reviews of ongoing decommissioning activities.

Specific events and findings are detailed in sections below.

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11. 2 . 2 Lepk from CarA9nktpel Piece oLPicina Durina Chemical Decontaminall9n Procou

a. Sspp_t

The inspector reviewed the circumstances that led to the identification of a seven gallon

per minute (gpm) leak from the cleanup system.

b. Observations and Findinos

On January 1,1998, beginning at 11:00 p.m., the primary coolant system leakage

increased from 0.37 gpm to 1 gpm, then to 4 gpm. Water was found running out of the

cleanup heat exchanger room. Operations isolated the cleanup system from the primary

system.

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The operators entered the heat exchanger room, removed lagging, and determined that

sample valve VC 2 was leaking through. The operators closed VC 14 (sample line

isolation valve) stopping the leak. Just prior to isolation, the leakage reached seven gpm.

The caute of the leak was failure by operations to identify a bypass line in the non-

regenerative heat exchanger with a sample valve had a stainless steel to carbon steel

reducer. A known smallleak through the threads of the carbon steal reducer was not well

communicated to the chemical decontamination team. The leak caused a flow path for

the hot flush chemical, which strongly attacks carbon steel. The chemical hot flush ate

the carbon steel threads away, resulting in the seven gpm leak.

c. Q9D0l uf]9D

'

The inspector concluded that a leaking valve allowed flow through an unidentified carbon

steel reducer, which was eaten away and resulted in a seven gpm leak during the

chemical hot flush.

II.3 Qgeommissionino Performance and Stojus Review f71801)

11. 3 . 1 Q&att.ej

The status of decommissioning, and licensee and contracted workforce conduct of

decommissioning activities in accordance with licensed requirements and crmmitments,

were evaluated. Control and conduct of facility decommissioning was exart ed to verify

the license and TS requirements and commitments described in the Final Hazard

Summary Report (FHSR) and PSDAR, were being met and implemented. Specific events

and findings are detailed in the section below.

a. Scope

Plant tours were performed by the inspectors to evaluate the materialintegrity of

structures, systems, and components necessary for the safe storage of spent fuel and

conduct of safe decommissioning, and to evaluate plant housekeeping and fire

protection.

b. Observations and Findinog

,

I

After conducting plant tours the inspectors brought minor concems to the plant manager's

l

attention. The plant staff then later resolved these concems. The inspector also

observed that plant management was actively monitoring plant housekeeping and fire

protection. When issues arose they were resolved. I

1

c. Conclusions

The inspector concluded that the material integrity of structures, systems, and

components necessary for the safe storage of spent fuel and conduct of safe

decommissioning was being maintained. Plant nousekeeping and fire protection were

generally good.

14

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.

111. Spent Fuel Safety ,

i

Ill.1 Qeneral J

,

The inspectors evaluated the performance or condition of structures, systems or I

components associated with storage, control, and maintenance of sperit fuelin a safe

manner.

111. 2 Spent Fuel Pool Spletv at Permanentiv Shut Down Reactors @001)

a. Scope

The inspect!on evaluated spent fuel and fuel pool safety. Factors considered in the

evaluation included: siphon and drain protection; SFP instrumentation, alarms, and  !

leakage detection; SFP chemistry and clean lIness control; criticality controls; and SFP ,

operation and power supply, t

b. Observations and Findinas

The only connection that can drain the fuel pool by siphoning is the cooling discherge

pipe, which retums water to the northwest comer of the fuel pool. The below surface

discharge was designed to minimize surface disturbance and improve visibility. To

prevent siphoning the water out of the pool, throo 7/16 inch holes were drilled just below

the water surface in the pipe. The licensee did not have any surveillance procedure to

document the condition of this siphon break. The licensee agreed to look into this issue.

Spent fuel pool instrumentation consists of level and temperature. Level is displayed in

the control room and recorded twice during a shift. Temperature indication is provided

locally at the S&Phooling water pump discharges, which is also recorded twice a shift.

These are adequaw to assure the safe storage of spent fuel. The licensee is planning to

provide level, temperature and new alarms for the new " control monitoring station".

Fuel pool leakage is monitored by eight tell tale drains from the area between the  ;

'

stainless steelliner and concrete. The tell tale leakage is recorded each shift with zero

leakage detected historically. There are severalindependent sources of makeup water to ,

the pool.

The Inspector observed that water chemistry and cleanliness controls were adequate.

The licensee maintains a cover over the pool. Criticality concems do not exist at this time

because fuel will not be moved until approved storage casks can be obtained.

Electrical power to req'uired systems has been supplied from essential buses since initial

design, and there are redundant supplies of water. Either the electrical or diesel fire

pumps can supply service water to the c, cling water heat exchanges if normal, non-

essential power is lost to the service water pumps.

The power supplies to the equipment used to cool the SFP are as follows:

e the primary source is the 138 Kv line, through the station transformer to the 1 A

bus and 2A bus

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_ _ _ _ _ _ _ - _ _ _ _ _ _ -

.

.

e the secondary source (following an automatic transfer) is the 46Kv line, througn

the station transformer, to the 1 A bus and 2A bus

e if neither the 138 KV nor the 46 KV line are available, the emergency diesst

generator automatically starts and energizes the 2B bus; after the 2B bus is

energized, the 1 A or 2A bus will be manually aligned to supply power to one of the

SFP pumps

e if for any reason the above three sources are unavailable, then the standby diesel

generator can be aligned to the 2B bus -

e the pumps required for cooling the SFP are spent fuel pit pump No.1 or No. 2,

reactor cooling water pumps No.1 or No. 2, and service water pumps No.1 or

No. 2. These pumps are all powered through the same primary and attemate

sources; the No.1 pumps are powered from the 1 A bus, and the No. 2 pumps are

powered from the 2B bus,

c. 9J2DgM!qu

The inspector concluded that the licensee can readily accommodate various conditions

that may challenge fuel pool level or cooling.

111. 3 Cold Weather Preparations (71714)

During a containment tour, the inspectors questioned the licensee on their contingency

plans for heating containment in the event that the main boiler is lost. The inspectors

were told that there was no contingency plans to supply additional heat to the

containment. The licensee stated that it would be good practice to have some sort of

program in place to maintain the temperature in the containment and/or respond if normal

heating is lost, and they agreed to waluate possible approaches to prevent the freezing

of systems which support the integrity of the fuel.

111. 4 Fuel Pool Activities (60710)

a. Scope

Review of the SFP cable log (which lists the weights and doses of items hanging from the

SFP rails) review of Field Monitoring Report FM-B-97129, and discussions with NPAD

inspectors, raised a concem that someone could inadvertently pull one of the high dose

items to the surface and receive a very high exposure,

b. Observatiqas and Findinas

Cables with high dose items hanging from them are hooked over the SFP rails. The

weight of the items varies from 12 pounds to 100-pounds. The dose of the items varies

from 3 R/hr to 1700 PJhr at one foot.

The potential for a high exposure from an individual pulling a high-dose item from the pool

was identified by NPAD and documented in FM B 97129. At the time of the inspection,

,

however, the licensee had not taken positive measures to prevent a person from

16

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.

Inadvertently pulling one of these items to the surface and receiving a very high exposure.

The inspector discussed this concem with plant management.

Management took immediate corrective action to place the SFP cover on the pool making

these cables inaccessible. On January 30,1998, a daily order was written stating the

covers need to be placed back over the SFP as soon as possible after any work is

performed that reduces removal of the covers. Positive controls for times when the SFP

covers must be removed and SFP activities resumed remain to be instituted. The

licensee's resolution of positive control over these cables in an inspector follow up item

(50155/97015 02(DNMS)).

c. GQncly119D

Positive controls are needed on high dose item suspended on cables in the SFP, to

prevent individuals from receiving a high exposure. The inspector communicated this

concem to plant management who had the covers put on the pool as a temporary

solution.

IV. Radiological Safety

IV.1 QQgypational Radiation Expp;ure (83750)

IV,1.1 General

Numerous aspects of licensee processes to mini.nize occupational radiation exposure

were selectively examined in order to evaluate overall radiation safety and to provide for

early identification of potential problems. Areas examined included: audits; planning and

preparation; extemal exposure control; intemal exposure control; control of radioactive

materials and contamination; surveys and monitonngs; and maintaining occupational

exposure as low as reasonably achievable (ALARA). Specific events and findings are

detailed in the sections below.

IV.1.2 Dose Monit9dag _urina Chemicpl Decontamination Process (837@)

a. Scop _q

The inspectors attended the pre-job and At. ARA briefings reviewed the RWP (B982035)

and Pre-job briefings signature sheet for January 4,1998, and held discussions with the

HP members of the HP department and the plant management.

b. Observatl0D! Lend Findinas

The inspectors observed the pre-job and Al. ARA briefing for the Chemical Decon (High

Radiation Area) RWP 8982053. During this briefing monitoring dosimetry and ensuring

that electronic dosimeters (ELD) were not on " pause" were discussed at length and were

stressed.

Daily, the RWP and pre-job briefing were reviewed with the workers and signed by them.

The written pre-job briefing requires that the worker monitor dosimetry every 15 minutes

when in a high radiation area.

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.

On January 4,1998, s' chemical decontamination worker read and signed RWP B982035

and was in a HRA for abou! 55 minutes.-

When the worket tried to log the ELD out, it was discovered that the ELD was on " pause,"-

l which was reported to the licensee; When the licensee interviewed the worker it was

learned that he had not checked his dosimetry every 15 minutes as required. Later, the

licensee determined that the workers ELD was faulty.- The worker was assigned a dose

of 6 mrom for the time he was in the HRA No exposure limits were exceeded.

The inspectors discussed this incident with the radiation protection manager and the plant

. manager, both of whom indicated that this behavior was not consistent with management

expectations for health physics practices. Plant management had counseled the worker

and his supervisor. Plant E-mail messages were sent to plant workers stressing the - o

need to ensure that ELDS are r'ot on : pause", i

The licensee's immediate corrective actions included the following:

.- The HP log-in book at the sphere will include the ELD reading in and out of the

sphere.

. The chemical decon supeivisor will review team member's ELD readings prior to

entry to the HRA at the chemical decontamination equipment area.

. The HP supervisor will tour a minimum of 3 times a shift, specifically reviewing

workers compliance with reading the ELD every 15 minutes while in a HRA.

. The ELDS and TLDs must be in clear plastic bags that allow monitoring of the

ELD reading while in a HRA.

. Briefing will remind workers of the expectations and requirements of monitoring

the ELD's reading once or twice an hour while in a radiation area and once every

15 minutes when in a HRA, This is a procedure requirement.

The licensee has had previous problems with workers being in the RCA with ELDS on

" pause" and the corrective actions and pre-job briefings did not prevent this incident. ,

Technical Specification 6.11 requires, in part, that procedures for personnel radiation -

protection shall be adhered to for all operations involving personnel radiation exposure. -

The written Pre-Job Briefing for Radiation Work Request (RWP B982035), and Procedure

5.5, " Radiation Work Permit," (Revision _12), instruct workers to monitor dosimetry every-

15 minutes when in e high radiation area. As described above. on January 4,1998, a

chemir.at decontamination worker was in a high radiation area (HRA) for greater than 15

minutes and did not inonitor his dosimetry. The worker was in the HRA about 55

minutes. Tnis is considered a violation (50-155/97015-03(DNMS)).

t

c. Conclusions l

A violation of Technical Specifications, concoming a decontamination worker in a HRA

not monitoring his dosimetry as required, and not noting that his ELD was on " pause,"

18

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.

Indicated that worker attention to radiatio 1 protection practices (especially in the area of

monitoring dosimetry), remained a problem for station perroml.

IV.2 Maintainina occupational Exposures ALARA (83750)

a. Scgge

The inspector reviewed the ALARA program for the chemical decontamination operation.

b. 90servations And Findinos

The chem decon of the reactor system and associated piping was done to reduce dose to

workers during plant dismantlement and represented a major Al. ARA initiative. The

licensee instituted several practicet to minimize dose since the solubilization and

transport of large quantities of isotopes in the reactor piping system would create the

potential for elevated radiation areas during the chem decon process. The licensee's

ALARA plan for dose minimization during the chem decon project was based on the

proven health physics practices of time, distance and shielding.

Temporary shielding in the form of standing water shields and lead blankets was

employed. Water shields were used to surround the ion exchange columns, lead

blankets were used in work areas as well as in localized and transient high radiation

areas. Low dose waiting areas (LOWA) were established for workers in the RCA during

pre-work activity and for equipm nt staging. Remote monitoring equipment includad area

radiation monitors (ARM), cameras and teledosimetry,

c. Conclusion

The chem decon project included appropriate dose-minimization planning, and effective

ALARA principles were implemented.

IV.3 Radiation Protection. Plant Chemistry and Radwaste(83722)

a. Scope

The inspetor reviewed the re 11ation protection (RP) program for the chemical

decontamination operation.

b. Observations And Findinas

The licensee instituted positive control over access to the containment sphere

during the chem decon process. Only personnel that were needed in the work

areas of the sphere were admitted. Access was controlled by use of a control

point outside of the sphere, a logbook, an access authorization list, locked rooms,

physical barricades, and radiation work permits (RWPs). Area radiation monitors

(ARMS) were placed in locations where elevated and changing dose rates would

be exp'cted from the transport of isotopes and crud bursts during the process.

Some areas where ARMS were located included the T-31 primary ion exchangers,

particulate filters, and the secondary lon exchangers. Significantly elevated dose

19

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.. . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

.

___

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'

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rates were expected from the T-31 primary ion exchangers, in addition to the

water shielding, these resin beds were located in an inaccessible area which was

posted and barricaded.

Change out of the particulate filters was perfo:Tned by hand instead of remote

equipment. The licensee and vendor evaluated dose rates with the filter housing

open and compared the time required for experienced technicians to remove the

filters against the time necessary to remove the filters by remote equipment. They

concluded that a manual filter change od would result in a lower total dose. The

initial filter change out resulted in a dose of only about 3g millirem to the technician

performing the job.

c. Conclusion

The licensee's radiation protection prograta for the chem decon process was well

planned and executed. Planning and communication, between licensee personnel

and the vendor performing the chem decon, were very good as was eviden.:ed by

the ALARA program, execution of the RP program during the process, and

adherence to the work schedule. .

V. Management Meeting

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on February 2,1998. The licensee acknowledged the

findings presented. The licensee stated that documents and processes associated with

- the chemical decontamination were considered proprietary; however, the inspector

described the expected contenta of the report and no use of proprietary information was

identified.

1

20

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.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

K Powers, General Manager

D. Hice, Plant Manager

K Pallegl, Radiation Protection and Environmental Manager

W. Trubliowicz, Scheduling and Project Control Manager

G. Withrow, Engineering Manager

D. Debner, Nuclear Fuel Projects Manager

C. Jurgens, Construction Manager

K Wooster, Emergency Planning Manager

M. VanAlst, Security Manager

L. Potter, Malntenance Supervisor

L. Darrah, Operations Supervisor

G. Hausler, Work Control Supervisor -

D. Lacroix, Training Supervisor

G. Rowell, Corrective Action Supervisor

M. Bourassa, Licensing Supervisor

G. Petijean, Senior Engineer (Altemate PRC Chairman)

E. Zionert, Human Resoure.es Director

T. Mosley, Senior Engineer Reactor Protection Projects

J. Corley, Nuclear Performance Assessment

L. Berry, Site Licensing Engineer

,

21

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INSPECTION PROCEDURES USED

36801- Organization, Wlanagement, and Cost Controls

37801 Safety Review, Design Changes, and Modifications

42700 Plant Procedures

60710 Fuel Handling Activities

60801 Spent Fuel Pool Safety at Permanently Shut Down Reactors

62801 Maintenance and Surveillance at Permanently Shutdown Reactors

71707 operational Safety Verification

71714 Cold Weather Preparations

71801 Decommissioning Performance and Status Review

-71801 - Decommissioning Performance and Status Reviews at Permanently Shut

Down Reactors

83722 Radiation Protection, Plant Chemistry and Radwaste

83750 Occupational Radiation Exposure

83750 Dose Monitoring During Chemical Decontamination Process

83750 Maintaining occupational Exposures ALARA

.92700. Onsite Follow-up, Written Reports of Non-routine Events at Power Reactor ~ ;

Facilities

22

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4

ITEMS OPENED AND CLOSED

QR10.td

.

50-155/97015-01 IFl - Licensee's resolution of flow induced vibration on damper

VHV 324

50-155/97015-02 IFl Licensee's resolution for positive control over cables

hanging in the SFP

50 155/97015-03 VIO Worker failed to monitor dosimetry while in a high radiation

arca

Reviewed but Remains Open

50-155/96002 VIO Control of combustible materials during outage related work

'

Closed

50-155/96006-03 IFl Sufficient core spray flow

- 50-155/9007-02 IN Delayed dispatch of operationa' support center emergency

response team

1

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.

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LIST OF ACROK'c4S USED

ALARA As Low As Reasonably Achievable

ARM Area radiation monitors

CFR Code of Federal Regulations

DNMS Div!sion of Nuclear Materials Safety

EDG Emergency diesel generator

ELD Electronic dosimetry

FEMA Federal Emergency Management Agency

FGEIS Final Generic Environment Impact Statement

FHSR- Final Hazard Summary Report

FM Field Monitoring

FSAR Final Safety Analysis Report

HEPA High Lificiency Padiculate Activity H5

HP Health Physics

HRA High Radiation Area

IFl inspector Follow-up item

LDWA Low dose waiting m 's

LTP License Terminatic lan

NPAD Nuclear Performar. Assessment Department

NRC Nuclear Reguls ory commission

"CM Offsite pose Calculation Manual

'

-Pct Public Document Room

PRC Piart 9afety Review Committee

PSDAR Post-Shutdown Decommissioning Activities Report

QA Quality Assurance -

Radwaste Radioactive Waste

RCS Reactor Coolant System

RP Radiation protection

RWP Radiation Work Request (RWP-Bg82035)

SAFESTOR Placing and maintaining a nuclear facility in a condition to safety store fuel

SFP- Spent Fuel Pool

SS Shift supervisor

SSCs Structures, Systems, and Components ,

'

TLD Thermal Luminescent Dosimeter

TS Technical Specification

TV Test Variable

USC Unreviewed Safety Question

,

24

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