IR 05000155/1996001

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Insp Rept 50-155/96-01 on 961019-1129.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20134C948
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 01/29/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20134C929 List:
References
50-155-96-01, 50-155-96-1, NUDOCS 9702040183
Download: ML20134C948 (21)


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I U.S. NUCLEAR REGULATORY COMISSION

REGION III

Docket No: 50-155 l

License No: DPR-06 Report No: 50-155/96010(DRP)

I Licensee: Consumers Power Company Facility: Big Rock Point Nuclear Power Plant Location: 10269 U.S. 31 North Charlevoix, MI 49720 Dates: October 19 - November 29, 1996 Inspectors: R. J. Leemon, Senior Resident Inspector C. E. Brown, Resident Inspector Approved by: Bruce L. Burgess, Chief Reactor Projects Branch 6 l

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gRo2040183 970129 G ADOCK 05000155 PDR l

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EXECUTIVE SUNIARY ,

l Big Rock Nuclear Power Plant NRC Inspection Report 50-155/96010 i This routine inspection covered aspects of licensee operations, engineering, j maintenance, and plant support.

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! Qgerations

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e The inspectors observed good operator performance, pre-job briefings,

! and engineer support during the shutdown on October 23 and the startup

on November 2, 1996. (Section 01.2)

! e An Operations Supervisor (OS) directed that the inlet valve to the  :

emergency condenser loop No. I be closed. The closure of the condenser i inlet valve rendered the condenser loop inoperable. The OS did not

recognize that the condenser loop was inoperable, and did not perform a
procedurally required surveillance on the other emergency condenser ,

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loop. One example of a violation of NRC requirements was identifie (Section 02.1)

i e The use of a procedure which did not ensure that modifications or

repairs required for cold weather protection were completed prior to the

, onset of cold weather was considered to be a violation of NRC i requirements. This was an inspector identified area of reoccurring l weaknes (Section 02.2)

i Maintenance

! e A good safety focus was maintained when performing the packing adjustment and stopping the steam leak on loop No.1 emergency condenser i inlet valve (M0-7062). The steam leak was stopped by backseating the

valve, which left the No.1 emergency condenser in service so that it l- could perform its safety related function of cooling the reactor if

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needed. (Section M2.1)

e The inspectors identified that the licensee used an informal process to ensure that required surveillances were performed within the specified frequenc Several procedural weaknesses were also noted. The inspectors identified to the licensee that a monthly surveillance test on the reactor depressurization system had not been completed on schedule, and that the TS grace period would be exceeded the next da As a result of the inspectors' questions, the licensee performed a review of past surveillances, and identified one example of a TS l required monthly surveillance which had not been completed within its I grace period. One violation was identifie (Section M3.1)

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Enaineerino e

The inspectors concluded that the engineering analysis (EA) work sheet which determined the maximum torque value for reactor depressurization

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i isolation valve packing gland nuts was adequate, based upon post '

maintenance test results. (Section E2.1)

e The licensee made operability determinations for a core spray isolation check valve and an emergency condenser loop which were subsequently reversed after review of the applicable portions of the FHSR. The inspectcrs considered these events to be indicative of a weakness in the licentas's use of the FHSR. (Section E3.1)

Plant Suonort e Two contractor workers in the decontamination facility unnecessarily contaminated themselves and previously uncontaminated portions of the ;

plant. The workers also fouled a fire barrier, and compensatory  !

measures were not established within the required time. Two violations I were identified. Licensee control of contractor activity had been identified in previous NRC inspection reports as an area of concer (Section R4.1).

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I Report Details Summary of Plant Status The plant was operated at full power from the beginning of the period until it i was shutdown on October 23, 1996, while the licensee verified that safety 4 related electrical equipment in the containment would operate in a postulated post accident environment. The licensee restarted the plant on November 2,

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and paralleled the generator to the grid on November 3. Full power was

attained on November 7, and the unit remained at power for the duration of the inspection period. The outage lasted 10 days and 19 hour2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> I. Operations 01 Conduct of Operations

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01.1 General Comments (71707)

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Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. The conduct of operations was professional and performed in a safety-conscious manner, except as discussed in section 02.1. Specific events and findings are detailed in the sections below.

01.2 Startuo and Shutdown Observations Inspection Scope The inspectors evaluated the licensee's activities during startup and shutdown using inspection module 71707, direct inspector observation, and conversation with plant personnel.

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b. Observations and Findinas

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. On October 23, 1996, the inspectors observed licensee staff perform a shutdown activities. The licensee performed a thorough crew briefing j prior to the start of the shutdown. This briefing covered the reason

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for the shutdown, the expected plant responses during the shutdown, and

the plant cool down rate to be established following the shutdown. On November 2, the licensee restarted the plant after an extensive and

! thorough reactivity briefing. Reactor criticality was achieved within j three control rod notches of the predicted position, as desire Both the shutdown and the startup were characterized by clear operator ;

communications, including the use of " repeat backs." Reactor l

. engineering provided attentive and effective oversight, and ensured that the operators understood each reactivity evolution. Additionally, the reactor engineers advised the operators of every reactivity high-worth ,

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control-rod notch prior to an operator manipulating the affected rod so that tne operator could keep the reactor period (rate of change of

. reactor power) within expected limit '

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. l The shift supervisors maintained effective control over both the i shutdown and the startup evolutions, and the operators used the

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appropriate procedures and control rod pull sheet '

c. Conclusion The inspectors observed good operator performance, pre-job bt !efings, i

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and engineer support during the shutdown on October 23 and the startup on November 2, 199 i 02 Operational Status of Facilities and Equipment 02.1 No.1 Emeraency Condenser looo Inlet Valve (M0-7062) Closed

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a. Insoection Scope

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The inspectors reviewed the licensee's response to a packing leak on the No. I emergency condenser loop inlet valve (M0-7062).

The inspectors held discussions with the shift supervisor, control room

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operators, and engineers. The inspectv s also reviewed station logs, daily orders, technical specifications (TS), the final hazards summary report (FHSR), and emergency condenser system (ECS) work order (WO) N .

b. Observations and Findinas l On November 7, 1996, with the unit at power, the licensee adjusted the valve stem packing nuts for M0-7062 in an attempt to stop a valve stem steam leak. The packing nuts were torqued to the maximum allowed value of 37 foot pounds; however, the steam leak continued. The operations supervisor (0S) then made the decision to close valve M0-7062 in an effort to reduce the stem leakage. The OS subsequently told the inspectors that he believed that M0-7062 would automatically reopen on an emergency signal, and that the safety function of M0-7062 was therefore not affected by the decision to close i Based on this assessment, the C5 considered the emergency condenser loop No. I to be operabl FHSR section 6.8.2 contained the following discussion on the operation of the emergency condenser: "The motor operated inlet valves are normally open during power operation and the motor operated outlet valves open in about 9 seconds and the system is in full operation within 20 to 30 seconds. In the event that one tube bundle is isolated, the operable tube bundle will operate as described within 30 second However, the motor operated inlet valve on the isolated loop requires about 31 seconds to open, thus the isolated, but serviceable, loop would come into service to remo.e decay heat in about 31 seconds as opposed to the 30 second minimum established for an operable loop. In the event one tube bundle is isolated but serviceable and the inlet valve is closed, AC power would be required to open the inlet valve, thus, on loss of station power only the outlet valve would open automatically and

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no steam flow would occur in this loop." The motor operator for M0-7062 was powered from a non-safety related 480 VAC bu Isolation of a leaking tube bundle loop was authorized by the T On November 8, the site head senior engineer was informed that M0-7062 was closed. The head senior engineer recognized that closing M0-7062 rendered emergency condenser loop No.1 inoperable, as discussed in . <1SR section 6.8.2. The licensee promptly reopened M0-7062, returning emergency condenser loop No. I to an operable status, and wrote condition report (CR) C-BRP-96-974, "M0-7062 Declared Operable in the Closed Position." Valve M0-7062 was in the closed position for 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> and 39 minute Procedure 50P-6, Volume 3, " Emergency Condenser System," Revision 154, step 2.2.b stated, "if one loop of the emergency condenser becomes inoperable, an operability test of the outlet valve on the other loop -

must be successfully completed within I hour."

The OS who directed that M0-7062 be closed told the inspectors that he had not tested the outlet valve on emergency condenser loop No. 2 because he considered emergency condenser loop No I to be operable. The ,

inspectors considered the failure to perform the operability test required by SOP-6, to be a vialation (50-155/96010-01(DRP)) of TS 6. c. Conclusion An Operations Supervisor (05) directed that the inlet valve to the emergency condenser loop No. 1 be closed. The closure of the condenser inlet valve rendered the condenser loop inoperable. The OS did not recognize that the condenser loop was inoperable, and as a result, did not perform a procedurally required surveillance on the other emergency condenser loop. One example of a violation of NRC requirements was identifie .2 Cold Weather Preparation (71714)

a. Inspection Scone The inspectors used inspection procedure 71714 to review the licensee's preparations for protection of safety-related systems from extreme cold weather. The inspection included a review of procedure 0-VAS-1,

" Cold / Warm Weather Checklists," revision 18; walkdowns of affected systems; and interviews with operations and maintenance department personne b. Observations and Findinas The inspectors noted that the operators had completed all sections of 0-VAS-1 for cold weather on October 25, and the operations manager had reviewed and signed the procedure on M ober 28, 1996. The inspectors performed walkdown verification that all the steps had been completed as directe __

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The inspector also reviewed 0-VAS-1 to ensure the correction of the

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following weaknesses which had been identified in Inspection Report 50-l 155/95011:

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1) The checklist only required that work 1rders for needed work had been submitted, it did not require that the work was actually completed prior to certifying the plant as ready for cold weathe ,

2) The checklist did not require verification that cold weather

)rotective measures had been re-established on all systems that

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l ind received maintenance-during the past year, nor did it require

! that proposed modifications to correct or enhance freeze l protection had been accomplished.

3) The procedure did not require that outstanding work requests on i affected systems be closed before signing the checklist as being complete. The failure to compete an outstanding work order on the stack gas monitoring system was the root cause for a previous violation (IR 155/93021-01).

The inspectors found that Revision 18 of 0-VAS-1 included a change to ensure that Naintenance had completed and signed for all work orders issued for performance of the checklist steps. However, the inspectors concluded that the procedure did not provide qualitative or quantitative criteria to ensure that required modifications or repairs were verified as complete, or otherwise dispositioned, prior to certification that the plant was prepared for cold weather. Continued use of a procedure which did not adequately ensure that required freeze protection measures were completed prior to the onset of cold weather was considered to be a violation (50-155/96010-02(DRP)) of 10 CFR 50, Appendix B, Criterion VAS-1, Attachment 2, " Cold Weather Checklist," required that the ,

waste-hold-tank (WHT) overflow-line heat tapes be placed in service by l checking that the supply breaker was closed and that the local indicator j light under the WHT was on. An operator closed the supply breaker, but 4 the indicating light did not come on. The operator verified that the 1 heat tapes were producing heat, noted the discrepancy on the check list, 1 and submitted work request (WR) No. 113742 to repair the' local  ;

indicating light on October 19, 1996. The shift supervisor (SS) ensured  !

that WR No. 113742 was listed in section 6.0, " Reviews," of 0-VAS-1 and signed the procedure off as reviewed on October 25, 1996. The operations manager signed the procedure off on October 28, 1996, before the indicating light had been repaire The inspector interviewed work control center personnel to determine the status of WR No. 113742. The interviews and a review t,f WR history revealed that WR No. 113742 had been canceled because it d viicated the intent of WR No. 111575, repair local heat-tape ind' 'ights, submitted on February 6, 1996. Actual work on WR f 3~ > was scheduled to start on November 13, after 0-VAS-1 was a off as complet _ _ __ _ _ __ . . __ __ _ __ . _. . ._ _

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l Although the safety-consequences of the local indicating light not

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operating were small (other means are available to ensure the heat trace tapes are operable), the inspectors considered this example to be

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illustrative of the need to review and disposition open freeze protection related work request ,

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, Conclusion l

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The use of a procedure which did not ensure that modifications or repairs required for cold weather protection were completed prior to the onset of cold weather was considered to be a violation of NRC requirements. This was an inspector identified area of reoccurring l weaknes !

02.3 Housekeepina - Plant Tours During plant tours, the inspectors noted that housekeeping was good.

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Cleanliness was maintained and passageways were kept clear. The ,

inspectors reported small discrepancies, such as an unattended ladder, '

i to the shift-supervisor (SS), who had them promptly corrected. However, one exception was noted. Three full 55-gallon barrels were left next to the post-incident test tank inside containment for more than a week after the inspectors had informed the SS about the seismic concerns involving the barre's. The barrels could have damaged recirculation

pump isolation $".,e instrumentation during a seismic event. After a i

week, the inspectors talked to another SS and the assistant plant

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manager who had the barrels move The inspectors noted that several lights were out in containment and i

verified that work requests had been submitted for each light. The inspector concluded that the operators were effectiveiv maintaining j II. Maintenance M1 Conduct of Maintenance M1.1 General Comments

, Inspection Scope (62703) (61726)

The inspectors observed all or portions of the following work activities:

Maintenance Activities a work t,rder (WO) RWS 12612094: install resin transfer pathway e WO RWS 12G12151: install resin transfer piping e WO SPS 12511883: inspect, repair circuit breaker 052-1E15 e WO EPS 12612145: repair emergency light unit No. 31 e WO EPS 12612143: repair emergency light unit No. 32 e W0 MBE 12611793: repair overhead lighting

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l e WO MBE 12612892: repair third floor lighting e WO SPS 12611938: periodic test electrical breaker 052-1A55 e WO SPS 12611939: periodic test electrical breaker 052-2A23 e WO MSS 12612329: adjust turbine bypass isolation valve (M0-7067)

packing leak e WO RDS 12612328: adjust reactor depressurization isolation valve

"D" (CV-4183) packing e WO ECS 12612287: adjust emergency condenser loop #1 inlet valve (M0-7062) packing

Surveillance Activities e T30-01
monthly reactor protection system test at power e OTGS-1: master checklist (for startup, shutdown, etc.)

e ORDS-7: reactor depressurization channel test, plant shutdown e TSD-01: fire pump operating characteristics e OVAS-1: cold / warm weather checklist e TR-43: shutdown margin check e T30-34: fire protection surveillance e T30-14: core spray heat exchanger leak test e T7-18: turbine bypass valve test b. Observations and Findinas Maintenance activities were normally thorough and satisfactorily performed. All observed work was performed with the work package present and in active use. Supervisors and system engineers monitored job progress, and appropriate radiation control measures were in plac When questions arose or problems were encountered, the workers stopped the activity and discussed the problems with management. Management then devised action plans to resolve the problems. Examples were the packing adjustment on the emergency condenser inlet valve (M0-7062), and the galled test tee on the vent line for differential pressure indication and switch (DPIS-7814). In addition, see M2 and M3 below for specific discussions of maintenance activities observe c. Conclusion All inspector observed maintenance and surveillance activities were correctly performed and accurately documente M2 Maintenance and Material Condition of Facilities and Equipment M2.1 Second Attemot to Tiahten Packina on Loon No. 1 Emeraency Condenser Inlet (M0-7062)

a. Inspection Scope

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The inspectors observed the interactions between licensee management and I

maintenance, engineering and operations personnel in resolving the l

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problem leaking valve stem packing on loop No.1 emergency condenser inlet valve (M0-7062). Observations and Findinas On November 27, 1996, for a second time, the licensee attempted to tighten the packing on loop No. I emergency condenser inlet valve (M0-7062). The first attempt was on November 07, 1996, (reference j section 02.1 of this report). The original torque value specified for i the packing gland nuts was 37 foot-pounds. During this second effort, i the packing gland was torqued to 60 foot pounds on one nut and 37 foot

pounds on the other nut. One side of the packing gland, even though it j was level, did not tighten u The licensee held discussions with the packing manufacturer who i

recommended leaving the valve on its backseat. The valve was torqued into the backseat with 70 foot pounds of force, an acceptable value as <

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calculated by the system engineers. The licensee then tightened the l

{ packing, and the valve was stroke tested electrically. The valve closed

and opened within the required stroke times. The licensee then

retorqued the valve into its backseat at 70 foot pounds, and the steam j leak stopped. The valve was declared inoperable, but because it was >

j open, the tube bundle remained operabl l l

l Conclusion i

! The licensee maintained a safety focus when working through the problem of the packing stem leak on loop No.1 emergency condenser inlet valve (M0-7062). The licensee stopped the steam leak by backseating the

valve. This left the No.1 emergency condenser in service so that it
could perform its safety functio l M3 Maintenance Procedures and Documentation l

! M3.1 Review of Licensee Scheduled and Comoleted Surveillance Trackina System

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l The inspectors reviewed the licensee's surveillance scheduling and i tracking system to determine if surveillances had been completed within 2 the required time frames. The inspectors reviewed: the operation's

! periodic test board from 1994,1995, and 1996; selected microfiche i

records of completed and non-completed surveillances; administrative

procedures; plant check sheets; a temporary change to 0-TGS-1 " Master

! Checklist," part B, section 3; condition report (CR) C-BRP-96-865 i " Violation of Technical Specification Surveillance;" and licensee event

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report (LER)96-011, " Technical Specification Surveillance Requirement Inadvertently Surpassed." The inspectors also held discussions with plant personnel, i

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b. Observations and Findinas A ground problem on Reactor Depressurization System (RDS) "B" (reference !

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inspection report 50-155/96008(DRP)) led the inspectors to perform an evaluation of the licensee's program for monitoring the completion of

, surveillance tests. Observations and findings are discussed belo Periodic Test Board i

The licensee used a periodic test board to track the status of -l

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surveillance tests. This board listed each required surveillance in a ;

row type format, and had columns for each scheduled performance of the l surveillance. The shift supervisor (SS) entered the date that the surveillance was completed on the periodic test board, or a notation why

, it wasn't completed. There was no formal process to ensure that l l surveillances which were not completed as scheduled were subsequently completed within the required frequency.

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Skinned Surveillances Not Adeauntely Tracked  :

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On September 19, 1996, the inspectors determined that the TS required i surveillance on RDS channel "A" had not been completed within the required 30-days, and would be outside its 25% grace period margin (allowed by TS 1.1.4) the following day. The inspectors notified the -

licensee, and the surveillance for RDS channel "A" (procedure T30-59)

was completed that day, within the grace perio T30-59 " Reactor Depressurization System Test at Power," was a monthly test that the licensee performed on one of four channels each wee '

When the plant was shutdown, the periodic test board was marked "SD" (shutdown) for the channel to be tested that week. When the plant was

.i re-started, the channel surveillance scheduled for the week of startup i

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was performed. Performing post-scheduled T30-59 surveillances for channels marked "SD" on the periodic test board was not always I j considered. This was the case with RDS channel "A" discussed abov I i The licensee performed a review of the periodic test boards for 1994, j

, 1995, and 1996 (through September), and a review of selective microfiche i 4 records. The inspectors performed a parallel review of this materia J

, The licensee determined that in March 1994 the monthly surveillance T30- l

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59 surveillance for RDS channel "C" was not completed until the 61st ;

l day. This occurred with the unit at power. The RDS channel "C" had j

passed its next surveillance test. The licensee initiated C-BRP-96-865 4 " Violation of Technical Specification Surveillance Requirements," and l

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wrote a LER. The failure to perform the RDS channel "C" surveillance j was a violation (VIO 50-155/96010-03) of Technical Specification j 11.4.1.5.

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Procedural Weaknesses The inspector identified a weakness in the startup check list 0-TGS-1

" Master Check List," revision 92, part B, section 3 " Preliminaries- l Putting Unit In-Service," in that step 1 stated " Check Periodic Test i Board Completed as Required." There was no criteria provided as to l which surveillances had to be shown as complete on the test board. In the inspector identified case involving RDS train "A" discussed above, ;

the need to perform a surveillance marked "SD" was not identified by the operator who completed startup check list 0-TGS- TGS-1 contained a step to verify RDS surveillances prior to start-u This step referenced 0-RDS-07, the test procedure for shut-down l conditions. 0-TGS-1 stated that if 0-RDS-07 had been completed within '

the last 90 days, it need not be done, and the step requiring its l performance was to be marked N/A. 0-TDS-1 did not reference T30-59, so '

if the plant was being returned to power following a short outage, the !

monthly surveillance requirement for the RDS, when operating, was not clearly identifie '

Licensee staff used green dots on the periodic test board to indicate which surveillances were not required to be performed when shutdow These surveillances were the ones which were found to be marked S !

However, procedure 2.12, " Operation's Documents," step 5.7, Periodic Test Board, did not address this proces !

Use of Grace Periods - 1 I

Some of the scheduled dates for completion of surveillances, as 1 identified on the periodic test board, exceeded the TS specified i frequency. The inspectors were informed that the licensee preferred to perform monthly surveillances on the same day of the same week each month (e.g. third thursday of each month). Because of the uneven number of weeks in a month, this scheduling method resulted in the potential scheduling of a monthly surveillance 35 days after the previous performance of that surveillance. The inspectors were concerned about the appropriateness of this use of grace period. The inspectors also noted that scheduled surveillances which used grace period (e.g. 30 day surveillance scheduled for completion on the 34th day) were not highlighted on the board. This made it difficult to determine whether a surveillance performed several days after it's scheduled date was within or outside the TS grace perio Additional Observations Surveillances which were not completed when scheduled on the test board were not highlighted or tracked on the board in any manner. There appeared to be no follow-through for surveillances that were not completed. There was no overview system for completed surveillances, and only a yearly management audit of the system was performe I

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The inspectors concluded, and the licensee subsequently acknowledged, that skill of the craft was being relied upon as a final barrier to i ensure that the RDS surveillance requirements were up to dat The inspectors found that the process for retrieval of completed surveillances was very time consuming. Surveillance procedures were maintained on microfiche and there was no hardcopy inder for the records. A computer system was used to determine the film cartridge number that the record was stored on. The inspectors were concerned that this process impeded plant staff in their efforts to track and trend surveillance result The inspectors concluded that the periodic test board was a poor record i of the completion of required surveillances because it was not well l defined in procedures, not well controlled in terms of data entry, no! I independently verified, and not maintained as a quality record after l use. Despite these problems, plant staff made extensive use of the '

board because of the difficulty in tracking the individual procedures which were the quality record of completed activitie Licensee Response to Inspectors' Observations The inspectors informed the licensee of their findings regarding skipped surveillances not being adequately tracked. In response, the licensee i made a temporary change to 0-TGS-1 " Master Checklist" part B, section 3, I step 42.b. This change stated, " Perform 0-RDS-7, reactor depressurization system channel test with the plant in shutdown, on any RDS channel that was not tested in accordance with T30-59, RDS channel test at power, while the plant was shutdown. This step is not-applicable if the RDS channels are being tested in accordance with T30-59 and the surveillance tests are current."

The licensee reviewed condition reports related to surveillance intervals not being met, and identified the following five examples of CRs written within the last three years:

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UPS batteries exceeded TS specified surveillance period, a LER had been submitte T30-59 for "A" RDS train performed in 37 versus 30 days (completed within 25 percent margin).

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T30-59 for "C" train exceeded TS specified surveillance period, a condition report and a LER were writte UPS batteries performed in 36 days versus 30 days (completed .

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Chemistry 90 day sampling requirement performed in 92 days versus 90 days (completed within 25 percent margin).

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c. Conclusion The inspectors identified that the licensee used an informal process to ensure that required surveillances were performed within the specified frequency. Several procedural weaknesses were also noted. The I inspectors identified to tb licensee that a monthly surveillance test ;

on the reactor depressurization system had not been completed on schedule, and that the TS grace period would be exceeded the next da As a result of the inspectors' questions, the licensee performed a review of past surveillances, and identified one example of a TS required monthly surveillance which had not been completed within its grace perio II. Enaineerina E2 Engineering Support of Facilities and Equipment E2.1 Enaineerina Evaluation to Increase Toroue Value for Packina Nuts on RDS Isolation Valves a. Scope  !

The inspector reviewed the engineering analysis (EA) work sheet for the evaluation of the maximum torque value for reactor depressurization isolation valve packing gland nuts, b. Observations and Findinal The EA documented an evaluation of the maximum torque limit for the packing gland follower nuts on the RDS (Anchor Darling) isolation valves. The original torque specification for the packing gland follower nuts was 41 foot-pounds. The licensee wanted to tighter. the packing gland nuts in order to stop packing gland leakage of primary coolant, and to prevent potential valve stem damage. Calculations were performed by the system engineers to keep the theoretical stem load below the force applied by the heavy springs which opened the valves on a RDS actuation. The evaluation determined that increasing the packing loading, without compromising valve stroke timing, was possible. The EA changed the gland follower nut torque valve from 41 foot-pounds to 180 foot-pounds. The analysis concluded that an increase of torque up to 180 foot-pounds would still permit valve RDS "D" CV-4183 to stroke freel '

On November 19, 1996, the packing gland follower nuts were torqued to 120 foot-pounds, which stopped the steam leak. Valve stroke time testing was accomplished per T90-07, "RDS Isolation Valve Test Operate at Power." The stroke time criteria of less than 4 seconds to open and less than 8 seconds to close were me l l

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! Conclusion j The inspectors concluded that the engineering analysis (EA) work sheet which determined the maximum torque value for reactor depressurization isolation valve "D" packing gland nuts was adequate, based upon post

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i maintenance test results.

E3 Engineering Procedures and Documentation E3.1 Licensee Operability Evaluations l

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i Scope The inspectors reviewed the related FHSR sections, held discussion with plant staff, and reviewed station logs to determine the appropriateness of two licensee operability evaluation Observations and Findinas Because of incomplete reviews of the FHSR, the licensee made poor operability calls on the following two occasions:

1) On August 27, 1996, (reference IR No. 50-155/96006, section M3.1)

the shift supervisor (SS), after discussion with management, declared VPI-303 (core spray to fire water system isolation check valve)

operable, despite a failed surveillance test. The surveillance test specified no allowable leakage, but a small amount of leakage past the valve had been foun FHSR Section 5.2.5.3.9, " Inter-system Leakage Detection" stated "Three systems interfacing with the reactor coolant pressure boundary (RCPB) at Big Rock Point are of concern and are monitored for signs of leakage: 1)

Liquid Poison System, 2) Core Spray / Fire System, and 3) Shutdown Cooling System."

The FHSR stated " Leakage to the core spray system is monitored by "tell-tale" lines installed between the motor operated valves in 1;oth core spray lines. Leakage from these "tell-tales" is monitored b/ auxiliary operators during bi-hourly rounds. Additionally, during monthly core-spray valve operability tests, leakage from these "tell-tales" is checked to ensure proper valve closure."

Later on August 27, the Plant Review Committee (PRC) determined that VPI-303 had to function as an inter-system LOCA valve as well as a backup core spray system check valve, based upon the FHSR sections referenced.above. The PRC then declared the valve inoperable because of the observed leakag ) On November 7,1996, the licensee closed and left closed emergency condenser loop No.1 inld valve (M0-7062) in hopes of reducing a valve stem packing leak (see section 02.1). The FHSR clearly stated that the motor operator for the inlet valve was supplied with non-vital power,

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, safety function if the inlet valve was closed. The OS who directed that M0-7062 be closed did not review the FHSR, and was not familiar with the referenced portion of the FHSR. As a result of this failure to review i the FHSR, the OS incorrectly classified the isolated emergency condenser ;

loop as being operable. This error was identified the following day, and the inlet valve was opened, returning the emergency condenser loop to an operable status

! Conclusion The licensee made operability determinations for a core spray isolation check valve and an emergency conden:er loop which were subsequently

reversed after review of the applicable portions of the FHSR. The

, inspectors considered these events to be indicative of a weakness in the ;

licensee's use of the FHS IV. P1 ant SuDDort

R1 Radiological Protection and Chemistry (RP&C) Controls j RI.1 General Comments j Using Inspection Procedures 71707 and 71750, the inspectors made i frequent tours of the radiologically protected area (RPA) and discussed i specific radiological controls with the ALARA coordinator and various  !

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radiation protection (RP) technicians. The inspectors observed plant conditions and licensee performance including radiation protection practices, and the compensatory measures taken by the licensee when radiation monitors were out of servic The inspectors concluded that the licensee was following good ALARA and radiation protection practices and performed the required compensatory measures when radiation monitors were cut of servic R4 Staff Knowledge and Performance in Radiological Protection and Chemistry Controls R Personnel Contamination of Contractor Employees Inspection Scope (71750)

The inspectors investigated the contractor and radiological controls that were in effect during a self-disclosing personnel contamination event involving contracted workers. The following documents were 1 reviewed:

e Administrative Procedure (AP) 3.2.3, " Control of Offsite Groups ,

Performing Maintenance Activities," Rev 4

  • AP 4.2.7, " Contracted Services," Rev 7

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e AP 4.4.7, " Fire Prevention Activities," Rev 7

i e AP 5.5, " Radiation Work Permit," Rev 7

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e LER 50-155/96005, " Fire Barrier Breach" LER 50-155/96006, " Fire Barrier Door Blocked by Ladder"

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e LER 50-155/96009, " Fire Barrier Breached by Air Hose" f

! Additionally, the inspectors interviewed the health physics manager, the <

ALARA coordinator, and the contractor forema Observations and Findinas

! During a plant tour on August 5,1996, the inspectors observed two

contractor personnel working on a contaminated pump in the plant i decontamination facility (DCF). The inspectors also observed a

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radiation protection (RP) technician providing periodic coverage and j assistance for the work. The inspectors again observed the workers in

! the DCF on the morning of August 7 but did not observe an RP technician or contract coordinator with the workers during the tour. Later that

day, the RP manager informed the inspectors that the two workers had

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been unable to pass through the personnel monitors (PCM-1Bs) when j attempting to exit the radiologically controlled area (RCA).

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The two workers had attempted to self-frisk and decontaminate areas on
heir clothing several times; however, the PCM-1Bs still alarmed for !

contamination on multiple areas of their bodies and clothing. Their '

escort (a licensee security guard) then called for an RP technician to l come to access control to assist the contract workers. The RP technician assessed the situation and notified his management, who took charge and directed further survey and decontamination efforts. Whole body counts of the two workers revealed that one of the workers had a contamination uptake (less than the action level of 100 nano-curies).

The RP manager restricted the two workers from access to the RC i The inspectors independently interviewed the contractor supervisor, the ALARA coordinator, and RP technicians to determine the facts surrounding this occurrence. The inspectors determined that the contractor supervisor had assigned the two workers to continue to repair the pump that they had been working on in the DCF the previous day. The ALARA coordinator, thinking they were going to be preparing for cleaning the resin dump tank room, had authorized the workers to use a general radiation work permit (RWP). The workers then signed in on the general RWP and proceeded to enter the DCF. The ALARA coordinator, who was also filling in for the contractor coordinator, later found the two contract-workers attempting to test run the pump with air supplied from a hose run through a fire door and across a contamination boundary. The ALARA coordinator stopped the work and told the two workers to clean up the area and exit from the RCA at that time. Neither the contract workers

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nor their escort had recognized that the hose was blocking the fire door. Additionally, there had been no RP coverage of the job during the time that the workers were working on the pump. Their actions had resulted in contaminating the area outside the contamination boundary to about 3000 disintegrations per minute (dpm)).

The inspectors determined that the two contractor workers had unnecessarily contaminated themselves and previously clean plant areas as a result of the use of poor contamination control practices and inadequate RP oversight. The failure to conform to proceduralized radiological protection program requirements was considered to be a violation (VIO 50-155/96010-04) of Technical Specification 6.1 The licensee determined that the fire barrier blocked by the airline was non-functional for approximately three hours. Rendering a fire barrier non-functional without implementing compensatory measures was considered 1 to be a violation (VIO 50-155/96010-05) of Technical Specification 12.3.7.1 The NRC had previously identified concerns with the plant's contractor control program in IR 50-155/95012. That report documented cases where a contractor worker cut a power cable with a backhoe, a contractor spilled contaminated resin in a secondary enclosure, and a contractor improperly assembled a dual-basket strainer in the supply to core spra In response to the NRC concerns, the licensee had committed to providing enhanced training to contractors (above that normally given in general employee training). Cor.clusion Two contractor workers in the decontamination facility unnecessarily contaminated themselves and previously uncontaminated portions of the ,

plant. The workers also fouled a fire barrier, and compensatory measures were not established within the required time. Two violations were identified. Licensee control of contractor activity had been identified in previous NRC inspection reports as an area of concer S1 Conduct of Security and Safeguards Activities S1.1 Security (71750) (71707)

The inspectors monitored the licensee's security program, during routine activities and tours, to ensure that the approved security plan was being implemented. The inspectors noted that persons within the protected area displayed proper photo-identification badges, and those individuals requiring escorts were properly escorted. The inspectors also observed that personnel and packages entering the protected area were searched by appropriate equipment or by han l 18  ;

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1 V. Manaaement Meetinas X1 Exit Meetina So-ary The inspectors presented the results of this inspection to members of licensee management on December 06, 1996. The licensee acknowledged the findings

presented. The licensee did not identify any of the documents or processes reviewed by the inspectors as being proprietary.

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PARTIAL LIST OF PERSONS CONTACTED Licensee P. Donnelly, Plant Manager R. Addy, Assistant Plant Manager S. Beachum, Systems and Project Engineering Manager ,

K. Pallagi, Chemistry / Health Physics Manager l L. Darrah, Operations Supervisor  :

D. Hice, Maintenance Manager l G. Withrow, Plant Safety and Licensing Director i INSPECTION PROCEDURES USED IP 37551: Engineering l IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and I Preventing Problems IP 61726: Surveillance Observations IP 62703: Maintenance Observation IP 71707: Plant Operations IP 71750: Plant Support Activities ITEMS OPENED and CLOSED Opened 155/96010-01 VIO M0-7062 closed without SOP-6 actions performed 155/96010-02 VIO cold / warm weather checklist sign off 155/96010-03 VIO failure to perform surveillance 155/96010-04 VIO poor contamination practices 155/96010-05 VIO fire barrier non-functional l

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l LIST OF ACRONYMS USED

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ALARA As Low As Reasonably Achievable A0 Auxiliary Operator i CFR Code of Federal Regulations l DRP Division of Reactor Projects '

FHSR Final Hazards Summary Report IFI Inspection Followup Item IP Inspection Procedure IR Inspection Report I LER Licensee Event Report NCV Non-Cited Violation NOV Notice of Violation NRC Nuclear Regulatory Commission RDS Reactor Depressurization System RP Radiation Protection RPA Radiologically Protected Area SS Shift Supervisor TS Technical Specification URI Unresolved Item VIO Violation W0 Work Order i

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