05000348/LER-1982-028: Difference between revisions

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| document report number = LER-82-028-03L, LER-82-28-3L, NUDOCS 8207090262
| document report number = LER-82-028-03L, LER-82-28-3L, NUDOCS 8207090262
| package number = ML20054M106
| package number = ML20054M106
| document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 1
| page count = 1
}}
}}

Latest revision as of 13:09, 15 March 2020

LER 82-028/03L-0:on 820605,during Performance of FNP-1-STP-22.16,turbine Driven Auxiliary Feedwater Pump Failed to Start.Caused by Faulty Limit Switch on Valve HV-3226.Limit Switch Replaced
ML20054M113
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/30/1982
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20054M106 List:
References
LER-82-028-03L, LER-82-28-3L, NUDOCS 8207090262
Download: ML20054M113 (1)


LER-2082-028,
Event date:
Report date:
3482082028R00 - NRC Website

text

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Il ~ill LICENSEE EVENT REPORT

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EVt'N1 DI.SCHIP llOtJ Aho PROB ACLE COW;EOUENCES eel [ At 0100 on 6-5-82 during_the_ performance of FNP-1-STP-2Ll6,_(Turbine _Drhenluxiliary_J gg] [Feedwater Pump Inservice Test), the Turbine Driven Auxiliary Feedwa_t.er Pump _was declaredj Egj [ inoperable when it failed to start. Tech. Spec. 3.7.1.22 in_ par _t, requires the lD_A_EW I t

} ggj [ pump to be operable. Tech. Spec. 3.7.1.2 action statement requirements were met. I g (Health / safety of the public was not affected. l EE]L_ _J eel" L__ J

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SE QUE N il AL OCCUR RE NCE HEFORT HEVISION

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44 41 CAU3E DESCHIPTION AND CCHRECTIVE AC~llONS .! /

EE] [This event was due to a faulty _ limit switch on valve HV_-3226 (Steam to TDAFW Pumq)_. j E[T] lThe limit switch was replaced and following the performance of FNP-1-STP-22.J6,_the _

I g;3 [TDAFW pump was declared operable at 1233 on 6-5-82. I eel 1 -

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_ Num o, Pnc enni n W. G. Hairston, I_II_ _ _ ., pnow (205L899-515_6_