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| | issue date = 05/09/1997 | | | issue date = 05/09/1997 |
| | title = LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr | | | title = LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr |
| | author name = HOVEY R J, KNORR J E | | | author name = Hovey R, Knorr J |
| | author affiliation = FLORIDA POWER & LIGHT CO. | | | author affiliation = FLORIDA POWER & LIGHT CO. |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:CATEGORY REGULATE INFORMATION DISTRIBUTION ST"M (RIDS)ACCES>ION NBR:9705160224 DOC.DATE: 97/05/09 NOTARIZED: | | {{#Wiki_filter:CATEGORY REGULATE INFORMATION DISTRIBUTION ST "M (RIDS) |
| NO ,I'ACIJ-::50-250 Turkey Point Plant, Unit 3, Florida Power and Light C AUTH.NAM".AUTHOR AFFILIATION
| | ACCES >ION NBR:9705160224 DOC.DATE: 97/05/09 NOTARIZED: NO DOCKET |
| 'NORR,J.E. | | ,I'ACIJ-::50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH.NAM" . AUTHOR AFFILIATION |
| Florida Power&L'ight Co.HOVEY,R.J. | | 'NORR,J.E. Florida Power & L'ight Co. |
| ~Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000250 | | HOVEY,R.J. ~ Florida Power & Light Co. |
| | RECIP.NAME RECIPIENT AFFILIATION |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER 97-004-00:on 970411,auxiliary feedwater automatic start upon trip of all main feedwater pumps, occurred.Caused by mispositioned valve closing.Valves listed as inappropriately positioned were repositioned.W/970509 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: C RECIPIENT ID CODE/NAME PD2-3 PD INTERNAL: AE D CE NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR COPIES LTTR ENCL 1 1 2'1, 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME CROTEAU,R AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB LITCO BRYCE,J H NOAC QUEENER,DS NUDOCS FULL TXT COPlES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 C NOTE TO ALL"RIDS" RECIPIENTS: | | LER 97-004-00:on 970411,auxiliary feedwater automatic start upon trip of all main feedwater pumps, occurred. Caused by mispositioned valve closing. Valves listed as inappropriately positioned were repositioned.W/970509 ltr. |
| PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROI DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24 I | | DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: |
| BAY 0 tggp L-97-125 10 CFR 550.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Re: Turkey Point Unit 3 Docket No.50-250 Reportable Event: 97-004-00 Auxiliary Feedwater Automatic Start The attached Licensee Event Report, 250/97-004-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv).
| | TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. |
| If there are any questions, please contact us.Very truly yours, R.J.Hove Vice President Turkey Point Plant JEK attachment cc: Luis A.Reyes, Regional Administrator, Region II, USNRC Thomas P.Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9705l60224
| | NOTES: |
| 'F70509 PDR ADOCK 05000250 8 PDR I QqlV<J'~lllllllllllllllllllllllllllllllfllllllll an FPL Group company
| | C RECIPIENT COPIES RECIPIENT COPlES C |
| | ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 PD 1 1 CROTEAU,R 1 1 AEOD/SPD/RRAB INTERNAL: AE CE D |
| | NRR/DE/EELB 1, |
| | 2 1 |
| | 1 1 |
| | NRR/DE/ECGB NRR/DE/EMEB 1 |
| | 1 1 |
| | 1 1 |
| | 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS: |
| | PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROI DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24 |
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| 'LICENSEE EVENT REPORT{LER}PACILITY NAME (1)TURKEY POINT UNIT 3 DOCKET NUMBER (2)05000250 PAGE (3)OF TITLE Auxiliary Feedwater Automatic Start Upon the Trip of all Main Feedwater Pumps MON DAY YR EVENT DATE (5)LER NUMBER(6)YR SEQ S RE MON DAY YR RPT DATE (7)OTHER FACILITIES INV.(8)PACILITY NAMES DOCKET S (S]97 OPERATING MODE (9)97 004 00 5 09 97 POWER LEVEL (10)N/A LICENSEE CONTACT FOR THIS LER{12)J.E.Knorr, Regulation and Compliance Specialist COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)TELEPHC"'UMBER 305-246-6757, CAUSE SYSTEM NPRDS?CAUSE SYSTEM MANUFACIURER NPRDS?SUPPLEMENTAL REPORT EXPECTED (14)NO YES 0 (If yes, complete EXPECTED SUBMISSION DATE)EXPECTED SUBMISSION DATE (15)MONTH DAY ABSTRACT (16)On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage.At 0503, while starting the 3B main feedwater pump (the 3A pump was off)the supply breaker failed to close.When the control switch was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied.
| | I BAY 0 tggp L-97-125 10 CFR 550.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 97-004-00 Auxiliary Feedwater Automatic Start The attached Licensee Event Report, 250/97-004-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv). |
| All auxiliary feedwater pumps started as expected.The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.The cause of the start failure of 3B main feedwater pump was found to be a mispositioned valve closing the sensing line for a start permissive lube oil pressure switch, resulting in a supply breaker not closing.Therefore the 3B main feedwater pump did not start which caused an auxiliary feedwater start.The cause of the mispositioned valve is indeterminate.
| | If there are any questions, please contact us. |
| The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.
| | Very truly yours, R. J. Hove Vice President Turkey Point Plant JEK attachment cc: Luis A. Reyes, Regional Administrator, Region II, USNRC Thomas P. Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9705l60224 'F70509 PDR ADOCK 05000250 8 PDR I QqlV<J'~ |
| | lllllllllllllllllllllllllllllllfllllllll an FPL Group company |
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| LICENSEE EAT REPORT (LER)TEXT fTINUATION FACILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.2 OF 5 I.DESCRIPTION OF LHE EVENT On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage and replacement of the 3B main feedwater pump casing.At 0503, while starting the first (3B)main feedwater pump[SJ:P]the supply breaker[SJ:BKR]failed to close.When the control switch[SJ:JS]was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. | | 'LICENSEE EVENT REPORT {LER} |
| All auxiliary feedwater pumps[BA:P]started as expected.The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.No other engineered safeguards equipment started or was expected to start.The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation. | | DOCKET NUMBER (2) PAGE (3) |
| II.SYSTEM DESCRIPTION Turkey Point Unit 3 has two main steam generator feedwater pumps which take water from the fifth stage of feedwater heaters and pump that water through the sixth stage of feedwater heaters into the steam generators.
| | PACILITY NAME (1) |
| The capacity of each of these pumps is enough to supply needed feed to the steam generators at 60%reactor power'.A successful startup of a main steam generator feedwater pump (closure of the electrical supply breaker)requires a number of system parameters to be met.1)Either the control switch in the control room or the local push button must be moved to the start position.2)The suction pressure to the pump must be greater than 240 psig.3)The lube oil pressure must'be greater than 7 psig.If all three of these conditions are not met the pump supply breaker will not close and start the main steam generator feedwater pump.The auxiliary feedwater system is designed to supply feed to the steam generators upon loss of normal feedwater. | | TURKEY POINT UNIT 3 05000250 OF TITLE Auxiliary Feedwater Automatic Start Upon the Trip of all Main Feedwater Pumps EVENT DATE (5) LER NUMBER(6) RPT DATE (7) OTHER FACILITIES INV. (8) |
| One of the five auxiliary feedwater actuation signals is the trip of both main steam generator feedwater pumps.Therefore, if an attempt is made to start the first steam generator feedwater pump and the pump does not start, releasing the control switch which will spring return to mid position, will actuate auxiliary feedwater.
| | MON DAY YR YR SEQ S RE MON DAY YR PACILITY NAMES DOCKET S (S] |
| This is what happened in this event.
| | 97 97 004 00 5 09 97 OPERATING MODE (9) |
| LICENSEE EAT REPORT (LER)TEXT PZINUATION
| | POWER LEVEL (10) N/A LICENSEE CONTACT FOR THIS LER {12) |
| 'ACILITY NAME TURKEY, POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.3 OF 5 III.CAUSE OF THE EVENT Investigation of the condition of the 3B main steam generator feedwater pump resulted in the identification of the isolation of the pressure switch (PS-3-2051)
| | TELEPHC"'UMBER J. E. Knorr, Regulation and Compliance Specialist 305-246-6757, COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| [SJ:63]for the lube oil pressure on the 3B feedwater pump.The isolation valve (3-40-097B)
| | CAUSE SYSTEM NPRDS? CAUSE SYSTEM MANUFACIURER NPRDS? |
| [SJ:ISV]for PS-3-2051 was found in the closed position.With this condition present, when the feedwater pump motor control switch was placed in the start position, the.pump did not start since the breaker did not close.The breaker did not close because'the pressure switch saw no lube oil pressure which prevented the breaker closure.The pressure switch must sense a lube oil pressure greater that 7 psig to enable the closure of the supply breaker.Investigation of the reasons for the closure of valve 3-40-097B found that the valve had been replaced during the refueling outage (March 23, 1997)and work order documentation indicated the valve was left in the open position.Two additional verifications of valve position were performed on March 31, 1997.Two other valves on the sensing lines for the suction side of the main steam generator feedwater pump were also found to be mispositioned.
| | SUPPLEMENTAL REPORT EXPECTED (14) NO YES 0 EXPECTED SUBMISSION MONTH DAY DATE (15) |
| 1)Valve 3-20-771[SJ:ISV], isolation valve for PS-3-2031, suction pressure start permissive
| | (If yes, complete EXPECTED SUBMISSION DATE) |
| [SJ:63]was found in the 1/4 turn open position.Full open for this valve requires 3 and 1/2, turns.Full closure of this valve would have prevented the start of the 3B main steam generator feedwater pump.2)Valve 3-20-765[SJ:ISV], high side isolation valve for the main steam generator f eedwater pump suction strainer differential pressure[SJ:PDS]was found closed instead of open.The as found condition of this valve would not have prevented the closure of the supply breaker to the 3B main steam generator feedwater pump.Each of these valves had been recently verified to be in their required position.The cause for the mispositioned valves is indeterminate.
| | ABSTRACT (16) |
| IV.ANALYSIS OF THE EVENT The loss of normal feedwater flow, is an analyzed event in the Updated Final Safety Analysis Report (UFSAR)(Section 14.1.11.1).
| | On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage. |
| | At 0503, while starting the 3B main feedwater pump ( the 3A pump was off) the supply breaker failed to close. When the control switch was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps started as expected. The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550. |
| | The cause of the start failure of 3B main feedwater pump was found to be a mispositioned valve closing the sensing line for a start permissive lube oil pressure switch, resulting in a supply breaker not closing. Therefore the 3B main feedwater pump did not start which caused an auxiliary feedwater start. The cause of the mispositioned valve is indeterminate. |
| | The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation. |
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| LICENSEE EM REPORT (LER)TEXT TINUATION'ACILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.4 OF 5 Following is a discussion of that analysis.A loss of normal feedwater results in a reduction in capability of the secondary system to remove heat generated in the reactor core.In the case of this event the reactor was in Mode 3 and had not started up since the shutdown for refueling on March 3, 1997.Therefore the heat in the core was limited to the remaining decay heat of the core and the heat generated by the running reactor coolant pumps.If an alternate supply of feedwater were not supplied to the plant, core residual heat could cause a primary system heatup.The residual heat in this event was minimal compared to the analyzed event.Three turbine driven auxiliary feedwater pumps start on the trip of all main feedwater pumps to supply feedwater to the s""am generators for continued heat removal from the reactor coolant system.The assumptions in the UFSAR accident analysis include initially operating at 102%reactor power with reactor coolant at 6 degrees Fahrenheit higher than nominal, and a reactor trip occurring on low-,low steam generator water level.All of these assumptions would result in more residual heat than that present in the event which is the subject of this Licensee Event Report.Analysis is presented in'he UFSAR to show that following a loss of normal feedwater, the auxiliary feedwater system is capable of removing the stored and residual heat, thus preventing either over pressurization of the reactor coolant system, over pressurization of the secondary side, or uncovery of the reactor core.Consequently, for the analyzed accident, the plant is able to return to a safe condition. | | LICENSEE EAT REPORT (LER) TEXT fTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO. |
| In this event no unsafe condition existed.Since the plant was tripped in Mode 3, and the steam generator heat transfer capability was not reduced, the primary system variables never approached a departure from nucleate boiling condition. | | TURKEY POINT UNIT 3 05000250 97-004-00 2 OF 5 I. DESCRIPTION OF LHE EVENT On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage and replacement of the 3B main feedwater pump casing. |
| Based on the above, the health"nd safety of the public were not adversely affected.V.CORRECTIVE ACTIONS 1)The valves listed as inappropriately positioned were repositioned. | | At 0503, while starting the first (3B) main feedwater pump [SJ:P] |
| | the supply breaker [SJ:BKR] failed to close. When the control switch [SJ:JS] was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps [BA:P] started as expected. The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550. No other engineered safeguards equipment started or was expected to start. |
| | The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation. |
| | II. SYSTEM DESCRIPTION Turkey Point Unit 3 has two main steam generator feedwater pumps which take water from the fifth stage of feedwater heaters and pump that water through the sixth stage of feedwater heaters into the steam generators. The capacity of each of these pumps is enough to supply needed feed to the steam generators at 60% |
| | reactor power'. A successful startup of a main steam generator feedwater pump (closure of the electrical supply breaker) requires a number of system parameters to be met. 1) Either the control switch in the control room or the local push button must be moved to the start position. 2) The suction pressure to the pump must be greater than 240 psig. 3) The lube oil pressure must'be greater than 7 psig. If all three of these conditions are not met the pump supply breaker will not close and start the main steam generator feedwater pump. |
| | The auxiliary feedwater system is designed to supply feed to the steam generators upon loss of normal feedwater. One of the five auxiliary feedwater actuation signals is the trip of both main steam generator feedwater pumps. Therefore, if an attempt is made to start the first steam generator feedwater pump and the pump does not start, releasing the control switch which will spring return to mid position, will actuate auxiliary feedwater. This is what happened in this event. |
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| | LICENSEE EAT REPORT (LER) TEXT PZINUATION |
| | 'ACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO. |
| | TURKEY, POINT UNIT 3 05000250 97-004-00 3 OF 5 III. CAUSE OF THE EVENT Investigation of the condition of the 3B main steam generator feedwater pump resulted in the identification of the isolation of the pressure switch (PS-3-2051) [SJ:63] for the lube oil pressure on the 3B feedwater pump. The isolation valve (3-40-097B) |
| | [SJ:ISV] for PS-3-2051 was found in the closed position. With this condition present, when the feedwater pump motor control switch was placed in the start position, the. pump did not start since the breaker did not close. The breaker did not close because 'the pressure switch saw no lube oil pressure which prevented the breaker closure. The pressure switch must sense a lube oil pressure greater that 7 psig to enable the closure of the supply breaker. |
| | Investigation of the reasons for the closure of valve 3-40-097B found that the valve had been replaced during the refueling outage (March 23, 1997) and work order documentation indicated the valve was left in the open position. Two additional verifications of valve position were performed on March 31, 1997. |
| | Two other valves on the sensing lines for the suction side of the main steam generator feedwater pump were also found to be mispositioned. |
| | : 1) Valve 3-20-771 [SJ:ISV], isolation valve for PS-3-2031, suction pressure start permissive [SJ:63] was found in the 1/4 turn open position. Full open for this valve requires 3 and 1/2, turns. Full closure of this valve would have prevented the start of the 3B main steam generator feedwater pump. |
| | : 2) Valve 3-20-765 [SJ:ISV], high side isolation valve for the main steam generator feedwater pump suction strainer differential pressure [SJ:PDS] was found closed instead of open. The as found condition of this valve would not have prevented the closure of the supply breaker to the 3B main steam generator feedwater pump. |
| | Each of these valves had been recently verified to be in their required position. |
| | The cause for the mispositioned valves is indeterminate. |
| | IV. ANALYSIS OF THE EVENT The loss of normal feedwater flow, is an analyzed event in the Updated Final Safety Analysis Report (UFSAR)(Section 14.1.11.1). |
| | |
| | LICENSEE EM REPORT (LER) TEXT TINUATION |
| | 'ACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO. |
| | TURKEY POINT UNIT 3 05000250 97-004-00 4 OF 5 Following is a discussion of that analysis. A loss of normal feedwater results in a reduction in capability of the secondary system to remove heat generated in the reactor core. In the case of this event the reactor was in Mode 3 and had not started up since the shutdown for refueling on March 3, 1997. Therefore the heat in the core was limited to the remaining decay heat of the core and the heat generated by the running reactor coolant pumps. |
| | If an alternate supply of feedwater were not supplied to the plant, core residual heat could cause a primary system heatup. |
| | The residual heat in this event was minimal compared to the analyzed event. |
| | Three turbine driven auxiliary feedwater pumps start on the trip of all main feedwater pumps to supply feedwater to the s""am generators for continued heat removal from the reactor coolant system. |
| | The assumptions in the UFSAR accident analysis include initially operating at 102 % reactor power with reactor coolant at 6 degrees Fahrenheit higher than nominal, and a reactor trip occurring on low-,low steam generator water level. All of these assumptions would result in more residual heat than that present in the event which is the subject of this Licensee Event Report. |
| | Analysis is presented in'he UFSAR to show that following a loss of normal feedwater, the auxiliary feedwater system is capable of removing the stored and residual heat, thus preventing either over pressurization of the reactor coolant system, over pressurization of the secondary side, or uncovery of the reactor core. Consequently, for the analyzed accident, the plant is able to return to a safe condition. In this event no unsafe condition existed. |
| | Since the plant was tripped in Mode 3, and the steam generator heat transfer capability was not reduced, the primary system variables never approached a departure from nucleate boiling condition. |
| | Based on the above, the health "nd safety of the public were not adversely affected. |
| | V. CORRECTIVE ACTIONS |
| | : 1) The valves listed as inappropriately positioned were repositioned. |
| | |
| | LICENSEE EAT REPORT (LER) TEKT PZINUATION |
| | 'ACIL'ITY NAME DOCKET NUMBER LER NUMBER PAGE NO. |
| | TURKEY POINT UNIT 3 05000250 97-004-00 5OF5 |
| | : 2) Starting alternatives to avoid auxiliary feedwater initiation upon failure of an initial main steam generator feedwater pump start will be evaluated. |
| | : 3) Procedure O-SMI-059.2, "Outside Containment Instrument Independent Verification Inspection," will be revised to include more explicit direction on how to ensure listed instruments are in service. This corrective action applies to both Units 3 and 4. |
| | : 4) Individuals responsible for verification of proper alignment of valves prior to pump operation were counseled. |
| | VI. ADDITIONAL INFORMATION EIIS "odes are shown in the format [EIIS SYSTEM: IEEE component function identifier, second component function identifier (if appropriate)j. |
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| LICENSEE EAT REPORT (LER)TEKT PZINUATION
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| 'ACIL'ITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.5OF5 2)Starting alternatives to avoid auxiliary feedwater initiation upon failure of an initial main steam generator feedwater pump start will be evaluated.
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| 3)Procedure O-SMI-059.2,"Outside Containment Instrument Independent Verification Inspection," will be revised to include more explicit direction on how to ensure listed instruments are in service.This corrective action applies to both Units 3 and 4.4)Individuals responsible for verification of proper alignment of valves prior to pump operation were counseled.
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| VI.ADDITIONAL INFORMATION EIIS"odes are shown in the format[EIIS SYSTEM: IEEE component function identifier, second component function identifier (if appropriate)j.
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
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CATEGORY REGULATE INFORMATION DISTRIBUTION ST "M (RIDS)
ACCES >ION NBR:9705160224 DOC.DATE: 97/05/09 NOTARIZED: NO DOCKET
,I'ACIJ-::50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH.NAM" . AUTHOR AFFILIATION
'NORR,J.E. Florida Power & L'ight Co.
HOVEY,R.J. ~ Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 97-004-00:on 970411,auxiliary feedwater automatic start upon trip of all main feedwater pumps, occurred. Caused by mispositioned valve closing. Valves listed as inappropriately positioned were repositioned.W/970509 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
C RECIPIENT COPIES RECIPIENT COPlES C
ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 PD 1 1 CROTEAU,R 1 1 AEOD/SPD/RRAB INTERNAL: AE CE D
NRR/DE/EELB 1,
2 1
1 1
NRR/DE/ECGB NRR/DE/EMEB 1
1 1
1 1
1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROI DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24
I BAY 0 tggp L-97-125 10 CFR 550.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 97-004-00 Auxiliary Feedwater Automatic Start The attached Licensee Event Report, 250/97-004-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv).
If there are any questions, please contact us.
Very truly yours, R. J. Hove Vice President Turkey Point Plant JEK attachment cc: Luis A. Reyes, Regional Administrator, Region II, USNRC Thomas P. Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9705l60224 'F70509 PDR ADOCK 05000250 8 PDR I QqlV<J'~
lllllllllllllllllllllllllllllllfllllllll an FPL Group company
'LICENSEE EVENT REPORT {LER}
DOCKET NUMBER (2) PAGE (3)
PACILITY NAME (1)
TURKEY POINT UNIT 3 05000250 OF TITLE Auxiliary Feedwater Automatic Start Upon the Trip of all Main Feedwater Pumps EVENT DATE (5) LER NUMBER(6) RPT DATE (7) OTHER FACILITIES INV. (8)
MON DAY YR YR SEQ S RE MON DAY YR PACILITY NAMES DOCKET S (S]
97 97 004 00 5 09 97 OPERATING MODE (9)
POWER LEVEL (10) N/A LICENSEE CONTACT FOR THIS LER {12)
TELEPHC"'UMBER J. E. Knorr, Regulation and Compliance Specialist 305-246-6757, COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM NPRDS? CAUSE SYSTEM MANUFACIURER NPRDS?
SUPPLEMENTAL REPORT EXPECTED (14) NO YES 0 EXPECTED SUBMISSION MONTH DAY DATE (15)
(If yes, complete EXPECTED SUBMISSION DATE)
ABSTRACT (16)
On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage.
At 0503, while starting the 3B main feedwater pump ( the 3A pump was off) the supply breaker failed to close. When the control switch was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps started as expected. The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.
The cause of the start failure of 3B main feedwater pump was found to be a mispositioned valve closing the sensing line for a start permissive lube oil pressure switch, resulting in a supply breaker not closing. Therefore the 3B main feedwater pump did not start which caused an auxiliary feedwater start. The cause of the mispositioned valve is indeterminate.
The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.
LICENSEE EAT REPORT (LER) TEXT fTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 97-004-00 2 OF 5 I. DESCRIPTION OF LHE EVENT On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage and replacement of the 3B main feedwater pump casing.
At 0503, while starting the first (3B) main feedwater pump [SJ:P]
the supply breaker [SJ:BKR] failed to close. When the control switch [SJ:JS] was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps [BA:P] started as expected. The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550. No other engineered safeguards equipment started or was expected to start.
The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.
II. SYSTEM DESCRIPTION Turkey Point Unit 3 has two main steam generator feedwater pumps which take water from the fifth stage of feedwater heaters and pump that water through the sixth stage of feedwater heaters into the steam generators. The capacity of each of these pumps is enough to supply needed feed to the steam generators at 60%
reactor power'. A successful startup of a main steam generator feedwater pump (closure of the electrical supply breaker) requires a number of system parameters to be met. 1) Either the control switch in the control room or the local push button must be moved to the start position. 2) The suction pressure to the pump must be greater than 240 psig. 3) The lube oil pressure must'be greater than 7 psig. If all three of these conditions are not met the pump supply breaker will not close and start the main steam generator feedwater pump.
The auxiliary feedwater system is designed to supply feed to the steam generators upon loss of normal feedwater. One of the five auxiliary feedwater actuation signals is the trip of both main steam generator feedwater pumps. Therefore, if an attempt is made to start the first steam generator feedwater pump and the pump does not start, releasing the control switch which will spring return to mid position, will actuate auxiliary feedwater. This is what happened in this event.
LICENSEE EAT REPORT (LER) TEXT PZINUATION
'ACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY, POINT UNIT 3 05000250 97-004-00 3 OF 5 III. CAUSE OF THE EVENT Investigation of the condition of the 3B main steam generator feedwater pump resulted in the identification of the isolation of the pressure switch (PS-3-2051) [SJ:63] for the lube oil pressure on the 3B feedwater pump. The isolation valve (3-40-097B)
[SJ:ISV] for PS-3-2051 was found in the closed position. With this condition present, when the feedwater pump motor control switch was placed in the start position, the. pump did not start since the breaker did not close. The breaker did not close because 'the pressure switch saw no lube oil pressure which prevented the breaker closure. The pressure switch must sense a lube oil pressure greater that 7 psig to enable the closure of the supply breaker.
Investigation of the reasons for the closure of valve 3-40-097B found that the valve had been replaced during the refueling outage (March 23, 1997) and work order documentation indicated the valve was left in the open position. Two additional verifications of valve position were performed on March 31, 1997.
Two other valves on the sensing lines for the suction side of the main steam generator feedwater pump were also found to be mispositioned.
- 1) Valve 3-20-771 [SJ:ISV], isolation valve for PS-3-2031, suction pressure start permissive [SJ:63] was found in the 1/4 turn open position. Full open for this valve requires 3 and 1/2, turns. Full closure of this valve would have prevented the start of the 3B main steam generator feedwater pump.
- 2) Valve 3-20-765 [SJ:ISV], high side isolation valve for the main steam generator feedwater pump suction strainer differential pressure [SJ:PDS] was found closed instead of open. The as found condition of this valve would not have prevented the closure of the supply breaker to the 3B main steam generator feedwater pump.
Each of these valves had been recently verified to be in their required position.
The cause for the mispositioned valves is indeterminate.
IV. ANALYSIS OF THE EVENT The loss of normal feedwater flow, is an analyzed event in the Updated Final Safety Analysis Report (UFSAR)(Section 14.1.11.1).
LICENSEE EM REPORT (LER) TEXT TINUATION
'ACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 97-004-00 4 OF 5 Following is a discussion of that analysis. A loss of normal feedwater results in a reduction in capability of the secondary system to remove heat generated in the reactor core. In the case of this event the reactor was in Mode 3 and had not started up since the shutdown for refueling on March 3, 1997. Therefore the heat in the core was limited to the remaining decay heat of the core and the heat generated by the running reactor coolant pumps.
If an alternate supply of feedwater were not supplied to the plant, core residual heat could cause a primary system heatup.
The residual heat in this event was minimal compared to the analyzed event.
Three turbine driven auxiliary feedwater pumps start on the trip of all main feedwater pumps to supply feedwater to the s""am generators for continued heat removal from the reactor coolant system.
The assumptions in the UFSAR accident analysis include initially operating at 102 % reactor power with reactor coolant at 6 degrees Fahrenheit higher than nominal, and a reactor trip occurring on low-,low steam generator water level. All of these assumptions would result in more residual heat than that present in the event which is the subject of this Licensee Event Report.
Analysis is presented in'he UFSAR to show that following a loss of normal feedwater, the auxiliary feedwater system is capable of removing the stored and residual heat, thus preventing either over pressurization of the reactor coolant system, over pressurization of the secondary side, or uncovery of the reactor core. Consequently, for the analyzed accident, the plant is able to return to a safe condition. In this event no unsafe condition existed.
Since the plant was tripped in Mode 3, and the steam generator heat transfer capability was not reduced, the primary system variables never approached a departure from nucleate boiling condition.
Based on the above, the health "nd safety of the public were not adversely affected.
V. CORRECTIVE ACTIONS
- 1) The valves listed as inappropriately positioned were repositioned.
LICENSEE EAT REPORT (LER) TEKT PZINUATION
'ACIL'ITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 97-004-00 5OF5
- 2) Starting alternatives to avoid auxiliary feedwater initiation upon failure of an initial main steam generator feedwater pump start will be evaluated.
- 3) Procedure O-SMI-059.2, "Outside Containment Instrument Independent Verification Inspection," will be revised to include more explicit direction on how to ensure listed instruments are in service. This corrective action applies to both Units 3 and 4.
- 4) Individuals responsible for verification of proper alignment of valves prior to pump operation were counseled.
VI. ADDITIONAL INFORMATION EIIS "odes are shown in the format [EIIS SYSTEM: IEEE component function identifier, second component function identifier (if appropriate)j.
0 I