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| issue date = 05/09/1997
| issue date = 05/09/1997
| title = LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr
| title = LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr
| author name = HOVEY R J, KNORR J E
| author name = Hovey R, Knorr J
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:CATEGORY REGULATE INFORMATION DISTRIBUTION ST"M (RIDS)ACCES>ION NBR:9705160224 DOC.DATE: 97/05/09 NOTARIZED:
{{#Wiki_filter:CATEGORY REGULATE     INFORMATION DISTRIBUTION           ST "M (RIDS)
NO ,I'ACIJ-::50-250 Turkey Point Plant, Unit 3, Florida Power and Light C AUTH.NAM".AUTHOR AFFILIATION
ACCES >ION NBR:9705160224           DOC.DATE:   97/05/09     NOTARIZED: NO              DOCKET
'NORR,J.E.
,I'ACIJ-::50-250     Turkey Point Plant, Unit 3, Florida           Power and   Light   C 05000250 AUTH.NAM"           . AUTHOR AFFILIATION
Florida Power&L'ight Co.HOVEY,R.J.
  'NORR,J.E.               Florida Power & L'ight Co.
~Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000250
HOVEY,R.J.       ~     Florida Power & Light Co.
RECIP.NAME             RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 97-004-00:on 970411,auxiliary feedwater automatic start upon trip of all main feedwater pumps, occurred.Caused by mispositioned valve closing.Valves listed as inappropriately positioned were repositioned.W/970509 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: C RECIPIENT ID CODE/NAME PD2-3 PD INTERNAL: AE D CE NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR COPIES LTTR ENCL 1 1 2'1, 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME CROTEAU,R AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB LITCO BRYCE,J H NOAC QUEENER,DS NUDOCS FULL TXT COPlES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 C NOTE TO ALL"RIDS" RECIPIENTS:
LER 97-004-00:on 970411,auxiliary feedwater automatic start upon trip of all main feedwater pumps, occurred. Caused by mispositioned valve closing. Valves listed as inappropriately positioned were repositioned.W/970509           ltr.
PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROI DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24 I
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR                   ENCL       SIZE:
BAY 0 tggp L-97-125 10 CFR 550.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Re: Turkey Point Unit 3 Docket No.50-250 Reportable Event: 97-004-00 Auxiliary Feedwater Automatic Start The attached Licensee Event Report, 250/97-004-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv).
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
If there are any questions, please contact us.Very truly yours, R.J.Hove Vice President Turkey Point Plant JEK attachment cc: Luis A.Reyes, Regional Administrator, Region II, USNRC Thomas P.Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9705l60224
NOTES:
'F70509 PDR ADOCK 05000250 8 PDR I QqlV<J'~lllllllllllllllllllllllllllllllfllllllll an FPL Group company
C RECIPIENT           COPIES            RECIPIENT            COPlES C
ID CODE/NAME         LTTR ENCL        ID CODE/NAME          LTTR ENCL PD2-3   PD               1    1      CROTEAU,R                1      1 AEOD/SPD/RRAB INTERNAL: AE CE D
NRR/DE/EELB 1,
2 1
1 1
NRR/DE/ECGB NRR/DE/EMEB 1
1 1
1 1
1 NRR/DRCH/HHFB              1     1     NRR/DRCH/HICB            1     1 NRR/DRCH/HOLB              1    1      NRR/DRCH/HQMB            1    1 NRR/DRPM/PECB              1    1      NRR/DSSA/SPLB            1    1 NRR/DSSA/SRXB              1    1      RES/DET/EIB               1     1 RGN2      FILE    01      1     1 EXTERNAL: L ST LOBBY WARD              1     1     LITCO BRYCE,J    H      1     1 NOAC POORE,W.              1     1     NOAC QUEENER,DS          1     1 NRC PDR                    1     1     NUDOCS FULL TXT          1     1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROI DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR               24   ENCL     24


'LICENSEE EVENT REPORT{LER}PACILITY NAME (1)TURKEY POINT UNIT 3 DOCKET NUMBER (2)05000250 PAGE (3)OF TITLE Auxiliary Feedwater Automatic Start Upon the Trip of all Main Feedwater Pumps MON DAY YR EVENT DATE (5)LER NUMBER(6)YR SEQ S RE MON DAY YR RPT DATE (7)OTHER FACILITIES INV.(8)PACILITY NAMES DOCKET S (S]97 OPERATING MODE (9)97 004 00 5 09 97 POWER LEVEL (10)N/A LICENSEE CONTACT FOR THIS LER{12)J.E.Knorr, Regulation and Compliance Specialist COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)TELEPHC"'UMBER 305-246-6757, CAUSE SYSTEM NPRDS?CAUSE SYSTEM MANUFACIURER NPRDS?SUPPLEMENTAL REPORT EXPECTED (14)NO YES 0 (If yes, complete EXPECTED SUBMISSION DATE)EXPECTED SUBMISSION DATE (15)MONTH DAY ABSTRACT (16)On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage.At 0503, while starting the 3B main feedwater pump (the 3A pump was off)the supply breaker failed to close.When the control switch was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied.
I BAY 0    tggp L-97-125 10 CFR 550.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington,       D. C. 20555 Re:      Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 97-004-00 Auxiliary Feedwater Automatic Start The attached Licensee Event Report, 250/97-004-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv).
All auxiliary feedwater pumps started as expected.The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.The cause of the start failure of 3B main feedwater pump was found to be a mispositioned valve closing the sensing line for a start permissive lube oil pressure switch, resulting in a supply breaker not closing.Therefore the 3B main feedwater pump did not start which caused an auxiliary feedwater start.The cause of the mispositioned valve is indeterminate.
If there        are any questions,          please contact us.
The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.  
Very    truly    yours, R. J. Hove Vice President Turkey Point Plant JEK attachment cc:      Luis A. Reyes, Regional Administrator, Region                        II, USNRC Thomas P. Johnson,        Senior Resident Inspector,                USNRC, Turkey Point Plant 9705l60224 'F70509 PDR      ADOCK    05000250 8                      PDR I QqlV<J'~
lllllllllllllllllllllllllllllllfllllllll an FPL Group company


LICENSEE EAT REPORT (LER)TEXT fTINUATION FACILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.2 OF 5 I.DESCRIPTION OF LHE EVENT On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage and replacement of the 3B main feedwater pump casing.At 0503, while starting the first (3B)main feedwater pump[SJ:P]the supply breaker[SJ:BKR]failed to close.When the control switch[SJ:JS]was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied.
                  'LICENSEE EVENT REPORT {LER}
All auxiliary feedwater pumps[BA:P]started as expected.The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.No other engineered safeguards equipment started or was expected to start.The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.
DOCKET NUMBER  (2)    PAGE  (3)
II.SYSTEM DESCRIPTION Turkey Point Unit 3 has two main steam generator feedwater pumps which take water from the fifth stage of feedwater heaters and pump that water through the sixth stage of feedwater heaters into the steam generators.
PACILITY NAME (1)
The capacity of each of these pumps is enough to supply needed feed to the steam generators at 60%reactor power'.A successful startup of a main steam generator feedwater pump (closure of the electrical supply breaker)requires a number of system parameters to be met.1)Either the control switch in the control room or the local push button must be moved to the start position.2)The suction pressure to the pump must be greater than 240 psig.3)The lube oil pressure must'be greater than 7 psig.If all three of these conditions are not met the pump supply breaker will not close and start the main steam generator feedwater pump.The auxiliary feedwater system is designed to supply feed to the steam generators upon loss of normal feedwater.
TURKEY POINT UNIT 3                                                 05000250                     OF TITLE    Auxiliary Feedwater Automatic Start                            Upon      the Trip of          all    Main Feedwater Pumps EVENT DATE  (5)        LER NUMBER(6)          RPT DATE  (7)            OTHER  FACILITIES INV. (8)
One of the five auxiliary feedwater actuation signals is the trip of both main steam generator feedwater pumps.Therefore, if an attempt is made to start the first steam generator feedwater pump and the pump does not start, releasing the control switch which will spring return to mid position, will actuate auxiliary feedwater.
MON      DAY      YR          YR    SEQ  S    RE    MON    DAY  YR                      PACILITY NAMES                DOCKET S  (S]
This is what happened in this event.
97         97    004       00     5      09    97 OPERATING MODE  (9)
LICENSEE EAT REPORT (LER)TEXT PZINUATION
POWER LEVEL (10)      N/A LICENSEE CONTACT FOR THIS LER {12)
'ACILITY NAME TURKEY, POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.3 OF 5 III.CAUSE OF THE EVENT Investigation of the condition of the 3B main steam generator feedwater pump resulted in the identification of the isolation of the pressure switch (PS-3-2051)
TELEPHC"'UMBER J. E. Knorr, Regulation and Compliance Specialist                                                                305-246-6757, COMPLETE ONE  LINE  FOR EACH COMPONENT FAILURE DESCRIBED  IN THIS  REPORT  (13)
[SJ:63]for the lube oil pressure on the 3B feedwater pump.The isolation valve (3-40-097B)
CAUSE    SYSTEM                                            NPRDS?      CAUSE      SYSTEM                    MANUFACIURER    NPRDS?
[SJ:ISV]for PS-3-2051 was found in the closed position.With this condition present, when the feedwater pump motor control switch was placed in the start position, the.pump did not start since the breaker did not close.The breaker did not close because'the pressure switch saw no lube oil pressure which prevented the breaker closure.The pressure switch must sense a lube oil pressure greater that 7 psig to enable the closure of the supply breaker.Investigation of the reasons for the closure of valve 3-40-097B found that the valve had been replaced during the refueling outage (March 23, 1997)and work order documentation indicated the valve was left in the open position.Two additional verifications of valve position were performed on March 31, 1997.Two other valves on the sensing lines for the suction side of the main steam generator feedwater pump were also found to be mispositioned.
SUPPLEMENTAL REPORT EXPECTED (14)    NO                YES 0                              EXPECTED SUBMISSION MONTH      DAY DATE  (15)
1)Valve 3-20-771[SJ:ISV], isolation valve for PS-3-2031, suction pressure start permissive
(If yes, complete EXPECTED SUBMISSION DATE)
[SJ:63]was found in the 1/4 turn open position.Full open for this valve requires 3 and 1/2, turns.Full closure of this valve would have prevented the start of the 3B main steam generator feedwater pump.2)Valve 3-20-765[SJ:ISV], high side isolation valve for the main steam generator f eedwater pump suction strainer differential pressure[SJ:PDS]was found closed instead of open.The as found condition of this valve would not have prevented the closure of the supply breaker to the 3B main steam generator feedwater pump.Each of these valves had been recently verified to be in their required position.The cause for the mispositioned valves is indeterminate.
ABSTRACT (16)
IV.ANALYSIS OF THE EVENT The loss of normal feedwater flow, is an analyzed event in the Updated Final Safety Analysis Report (UFSAR)(Section 14.1.11.1).  
On   April     11, 1997,       Florida         Power     E   Light Company's Turkey Point Unit                           3   was in   Mode 3     proceeding toward               a   startup following a refueling outage.
At 0503, while starting the 3B main feedwater pump ( the 3A pump was off) the supply breaker failed to close. When the control switch was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps started as expected.                         The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.
The cause        of the start failure of 3B main feedwater pump was found to be a mispositioned valve closing the sensing line for a start permissive lube oil pressure switch, resulting in a supply breaker not closing. Therefore the 3B main feedwater pump did not start which caused an auxiliary feedwater start. The cause of the mispositioned valve is indeterminate.
The NRC      operations center                was    notified at        0832      in accordance with              10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.


LICENSEE EM REPORT (LER)TEXT TINUATION'ACILITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.4 OF 5 Following is a discussion of that analysis.A loss of normal feedwater results in a reduction in capability of the secondary system to remove heat generated in the reactor core.In the case of this event the reactor was in Mode 3 and had not started up since the shutdown for refueling on March 3, 1997.Therefore the heat in the core was limited to the remaining decay heat of the core and the heat generated by the running reactor coolant pumps.If an alternate supply of feedwater were not supplied to the plant, core residual heat could cause a primary system heatup.The residual heat in this event was minimal compared to the analyzed event.Three turbine driven auxiliary feedwater pumps start on the trip of all main feedwater pumps to supply feedwater to the s""am generators for continued heat removal from the reactor coolant system.The assumptions in the UFSAR accident analysis include initially operating at 102%reactor power with reactor coolant at 6 degrees Fahrenheit higher than nominal, and a reactor trip occurring on low-,low steam generator water level.All of these assumptions would result in more residual heat than that present in the event which is the subject of this Licensee Event Report.Analysis is presented in'he UFSAR to show that following a loss of normal feedwater, the auxiliary feedwater system is capable of removing the stored and residual heat, thus preventing either over pressurization of the reactor coolant system, over pressurization of the secondary side, or uncovery of the reactor core.Consequently, for the analyzed accident, the plant is able to return to a safe condition.
LICENSEE       EAT    REPORT     (LER) TEXT     fTINUATION FACILITY NAME                 DOCKET NUMBER      LER NUMBER          PAGE NO.
In this event no unsafe condition existed.Since the plant was tripped in Mode 3, and the steam generator heat transfer capability was not reduced, the primary system variables never approached a departure from nucleate boiling condition.
TURKEY POINT UNIT 3            05000250          97-004-00          2 OF 5 I. DESCRIPTION OF LHE EVENT On  April  11,  1997,  Florida  Power    E Light  Company's    Turkey Point Unit 3 was in Mode 3 proceeding toward                a startup following a refueling outage and replacement of the              3B main feedwater pump casing.
Based on the above, the health"nd safety of the public were not adversely affected.V.CORRECTIVE ACTIONS 1)The valves listed as inappropriately positioned were repositioned.  
At 0503, while starting the first (3B) main feedwater pump [SJ:P]
the supply breaker [SJ:BKR] failed to close.                  When the control switch [SJ:JS] was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps [BA:P] started as expected.        The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550. No other engineered safeguards equipment started or was expected to start.
The NRC  operations center      was  notified at  0832    in accordance with 10 CFR  550.72(b)(2)(ii), Engineered Safety Feature Actuation.
II. SYSTEM DESCRIPTION Turkey Point Unit 3 has two main steam generator feedwater pumps which take water from the fifth stage of feedwater heaters and pump that water through the sixth stage of feedwater heaters into the steam generators.        The capacity of each of these pumps is enough to supply needed feed to the steam generators at 60%
reactor  power'. A successful startup of a main steam generator feedwater pump (closure of the electrical supply breaker) requires a number of system parameters to be met. 1) Either the control switch in the control room or the local push button must be moved to the start position.            2) The suction pressure to the pump must be greater than 240 psig.            3) The lube oil pressure must'be greater than 7 psig. If all three of these conditions are not met the pump supply breaker will not close and start the main steam generator feedwater pump.
The  auxiliary feedwater      system  is  designed to supply feed to the steam generators upon loss of normal feedwater.                One of the five auxiliary feedwater actuation signals is the trip of both main steam generator feedwater pumps. Therefore,              if  an attempt is made to start the first steam generator feedwater pump and the pump does not start, releasing the control switch which will spring return to mid position, will actuate auxiliary feedwater. This is what happened in this event.
 
LICENSEE    EAT REPORT        (LER) TEXT PZINUATION
'ACILITY NAME                DOCKET NUMBER     LER NUMBER     PAGE NO.
TURKEY, POINT UNIT 3          05000250        97-004-00       3 OF 5 III. CAUSE    OF THE EVENT Investigation of the condition of the 3B main steam generator feedwater pump resulted in the identification of the isolation of the pressure switch (PS-3-2051) [SJ:63] for the lube oil pressure on the 3B feedwater pump. The isolation valve (3-40-097B)
[SJ:ISV] for PS-3-2051 was found in the closed position. With this condition present, when the feedwater pump motor control switch was placed in the start position, the. pump did not start since the breaker did not close. The breaker did not close because 'the pressure switch saw no lube oil pressure which prevented the breaker closure. The pressure switch must sense a lube oil pressure greater that 7 psig to enable the closure of the supply breaker.
Investigation of the reasons for the closure of valve 3-40-097B found that the valve had been replaced during the refueling outage (March 23, 1997) and work order documentation indicated the valve was left in the open position. Two additional verifications of valve position were performed on March 31, 1997.
Two  other valves on the sensing lines for the suction side of the main steam generator feedwater pump were also found to be mispositioned.
: 1)  Valve 3-20-771 [SJ:ISV], isolation valve for PS-3-2031, suction pressure start permissive [SJ:63] was found in the 1/4 turn open position. Full open for this valve requires 3 and 1/2, turns. Full closure of this valve would have prevented the start of the 3B main steam generator feedwater pump.
: 2) Valve 3-20-765    [SJ:ISV], high side isolation valve for the main steam generator feedwater pump suction strainer differential pressure [SJ:PDS] was found closed instead of open. The as found condition of this valve would not have prevented the closure of the supply breaker to the 3B main steam generator feedwater pump.
Each  of these valves  had been  recently verified to be in their required position.
The cause    for the mispositioned valves is indeterminate.
IV. ANALYSIS OF THE EVENT The  loss of normal feedwater flow, is an analyzed event in the Updated Final Safety Analysis Report (UFSAR)(Section 14.1.11.1).
 
LICENSEE    EM REPORT          (LER) TEXT    TINUATION
'ACILITY NAME                DOCKET NUMBER    LER NUMBER      PAGE NO.
TURKEY POINT UNIT 3            05000250        97-004-00      4 OF 5 Following is a discussion of that analysis. A loss of normal feedwater results in a reduction in capability of the secondary system to remove heat generated in the reactor core.         In the case of this event the reactor was in Mode 3 and had not started up since the shutdown for refueling on March 3, 1997. Therefore the heat in the core was limited to the remaining decay heat of the core and the heat generated by the running reactor coolant pumps.
If an alternate supply of feedwater were not supplied to the plant, core residual heat could cause a primary system heatup.
The residual heat in this event was minimal compared to the analyzed event.
Three turbine driven auxiliary feedwater pumps start on the trip of all main feedwater pumps to supply feedwater to the s""am generators for continued heat removal from the reactor coolant system.
The assumptions in     the UFSAR accident analysis include initially operating at 102 %     reactor power with reactor coolant at 6 degrees Fahrenheit higher than nominal, and a reactor trip occurring on low-,low steam generator water level. All of these assumptions would result in more residual heat than that present in the event which is the subject of this Licensee Event Report.
Analysis is presented in'he UFSAR to show that following a loss of normal feedwater, the auxiliary feedwater system is capable of removing the stored and residual heat, thus preventing either over pressurization of the reactor coolant system, over pressurization of the secondary side, or uncovery of the reactor core. Consequently, for the analyzed accident, the plant is able to return to a safe condition. In this event no unsafe condition existed.
Since the plant was tripped in Mode 3, and the steam generator heat transfer capability was not reduced, the primary system variables never approached a departure from nucleate boiling condition.
Based on the above,     the health "nd safety of the public were not adversely affected.
V. CORRECTIVE ACTIONS
: 1)   The valves   listed as inappropriately positioned were repositioned.
 
LICENSEE      EAT REPORT        (LER) TEKT PZINUATION
'ACIL'ITY NAME                DOCKET NUMBER    LER NUMBER      PAGE NO.
TURKEY POINT UNIT 3            05000250        97-004-00      5OF5
: 2)    Starting alternatives to avoid auxiliary feedwater initiation upon failure of an initial main steam generator feedwater    pump start will be evaluated.
: 3)    Procedure O-SMI-059.2, "Outside Containment Instrument Independent Verification Inspection," will be revised to include more explicit direction on how to ensure listed instruments are in service. This corrective action applies to both Units 3 and 4.
: 4)    Individuals responsible for verification of proper alignment of valves prior to pump operation were counseled.
VI. ADDITIONAL INFORMATION EIIS "odes are shown in the format [EIIS        SYSTEM: IEEE component function identifier,    second component    function identifier  (if appropriate)j.


LICENSEE EAT REPORT (LER)TEKT PZINUATION
'ACIL'ITY NAME TURKEY POINT UNIT 3 DOCKET NUMBER 05000250 LER NUMBER 97-004-00 PAGE NO.5OF5 2)Starting alternatives to avoid auxiliary feedwater initiation upon failure of an initial main steam generator feedwater pump start will be evaluated.
3)Procedure O-SMI-059.2,"Outside Containment Instrument Independent Verification Inspection," will be revised to include more explicit direction on how to ensure listed instruments are in service.This corrective action applies to both Units 3 and 4.4)Individuals responsible for verification of proper alignment of valves prior to pump operation were counseled.
VI.ADDITIONAL INFORMATION EIIS"odes are shown in the format[EIIS SYSTEM: IEEE component function identifier, second component function identifier (if appropriate)j.
0 I}}
0 I}}

Latest revision as of 21:16, 3 February 2020

LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr
ML17354A505
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 05/09/1997
From: Hovey R, Knorr J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-97-125, LER-97-004-01, LER-97-4-1, NUDOCS 9705160224
Download: ML17354A505 (13)


Text

CATEGORY REGULATE INFORMATION DISTRIBUTION ST "M (RIDS)

ACCES >ION NBR:9705160224 DOC.DATE: 97/05/09 NOTARIZED: NO DOCKET

,I'ACIJ-::50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH.NAM" . AUTHOR AFFILIATION

'NORR,J.E. Florida Power & L'ight Co.

HOVEY,R.J. ~ Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 97-004-00:on 970411,auxiliary feedwater automatic start upon trip of all main feedwater pumps, occurred. Caused by mispositioned valve closing. Valves listed as inappropriately positioned were repositioned.W/970509 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

C RECIPIENT COPIES RECIPIENT COPlES C

ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 PD 1 1 CROTEAU,R 1 1 AEOD/SPD/RRAB INTERNAL: AE CE D

NRR/DE/EELB 1,

2 1

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I BAY 0 tggp L-97-125 10 CFR 550.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 97-004-00 Auxiliary Feedwater Automatic Start The attached Licensee Event Report, 250/97-004-00, is being provided in accordance with 10 CFR 50.73(a)(2)(iv).

If there are any questions, please contact us.

Very truly yours, R. J. Hove Vice President Turkey Point Plant JEK attachment cc: Luis A. Reyes, Regional Administrator, Region II, USNRC Thomas P. Johnson, Senior Resident Inspector, USNRC, Turkey Point Plant 9705l60224 'F70509 PDR ADOCK 05000250 8 PDR I QqlV<J'~

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'LICENSEE EVENT REPORT {LER}

DOCKET NUMBER (2) PAGE (3)

PACILITY NAME (1)

TURKEY POINT UNIT 3 05000250 OF TITLE Auxiliary Feedwater Automatic Start Upon the Trip of all Main Feedwater Pumps EVENT DATE (5) LER NUMBER(6) RPT DATE (7) OTHER FACILITIES INV. (8)

MON DAY YR YR SEQ S RE MON DAY YR PACILITY NAMES DOCKET S (S]

97 97 004 00 5 09 97 OPERATING MODE (9)

POWER LEVEL (10) N/A LICENSEE CONTACT FOR THIS LER {12)

TELEPHC"'UMBER J. E. Knorr, Regulation and Compliance Specialist 305-246-6757, COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAUSE SYSTEM NPRDS? CAUSE SYSTEM MANUFACIURER NPRDS?

SUPPLEMENTAL REPORT EXPECTED (14) NO YES 0 EXPECTED SUBMISSION MONTH DAY DATE (15)

(If yes, complete EXPECTED SUBMISSION DATE)

ABSTRACT (16)

On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage.

At 0503, while starting the 3B main feedwater pump ( the 3A pump was off) the supply breaker failed to close. When the control switch was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps started as expected. The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550.

The cause of the start failure of 3B main feedwater pump was found to be a mispositioned valve closing the sensing line for a start permissive lube oil pressure switch, resulting in a supply breaker not closing. Therefore the 3B main feedwater pump did not start which caused an auxiliary feedwater start. The cause of the mispositioned valve is indeterminate.

The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.

LICENSEE EAT REPORT (LER) TEXT fTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY POINT UNIT 3 05000250 97-004-00 2 OF 5 I. DESCRIPTION OF LHE EVENT On April 11, 1997, Florida Power E Light Company's Turkey Point Unit 3 was in Mode 3 proceeding toward a startup following a refueling outage and replacement of the 3B main feedwater pump casing.

At 0503, while starting the first (3B) main feedwater pump [SJ:P]

the supply breaker [SJ:BKR] failed to close. When the control switch [SJ:JS] was returned to the mid position, with no other main feedwater pump running, the logic for automatic auxiliary feedwater start was satisfied. All auxiliary feedwater pumps [BA:P] started as expected. The auxiliary feedwater pumps were shutdown and returned to normal standby status at 0550. No other engineered safeguards equipment started or was expected to start.

The NRC operations center was notified at 0832 in accordance with 10 CFR 550.72(b)(2)(ii), Engineered Safety Feature Actuation.

II. SYSTEM DESCRIPTION Turkey Point Unit 3 has two main steam generator feedwater pumps which take water from the fifth stage of feedwater heaters and pump that water through the sixth stage of feedwater heaters into the steam generators. The capacity of each of these pumps is enough to supply needed feed to the steam generators at 60%

reactor power'. A successful startup of a main steam generator feedwater pump (closure of the electrical supply breaker) requires a number of system parameters to be met. 1) Either the control switch in the control room or the local push button must be moved to the start position. 2) The suction pressure to the pump must be greater than 240 psig. 3) The lube oil pressure must'be greater than 7 psig. If all three of these conditions are not met the pump supply breaker will not close and start the main steam generator feedwater pump.

The auxiliary feedwater system is designed to supply feed to the steam generators upon loss of normal feedwater. One of the five auxiliary feedwater actuation signals is the trip of both main steam generator feedwater pumps. Therefore, if an attempt is made to start the first steam generator feedwater pump and the pump does not start, releasing the control switch which will spring return to mid position, will actuate auxiliary feedwater. This is what happened in this event.

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'ACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY, POINT UNIT 3 05000250 97-004-00 3 OF 5 III. CAUSE OF THE EVENT Investigation of the condition of the 3B main steam generator feedwater pump resulted in the identification of the isolation of the pressure switch (PS-3-2051) [SJ:63] for the lube oil pressure on the 3B feedwater pump. The isolation valve (3-40-097B)

[SJ:ISV] for PS-3-2051 was found in the closed position. With this condition present, when the feedwater pump motor control switch was placed in the start position, the. pump did not start since the breaker did not close. The breaker did not close because 'the pressure switch saw no lube oil pressure which prevented the breaker closure. The pressure switch must sense a lube oil pressure greater that 7 psig to enable the closure of the supply breaker.

Investigation of the reasons for the closure of valve 3-40-097B found that the valve had been replaced during the refueling outage (March 23, 1997) and work order documentation indicated the valve was left in the open position. Two additional verifications of valve position were performed on March 31, 1997.

Two other valves on the sensing lines for the suction side of the main steam generator feedwater pump were also found to be mispositioned.

1) Valve 3-20-771 [SJ:ISV], isolation valve for PS-3-2031, suction pressure start permissive [SJ:63] was found in the 1/4 turn open position. Full open for this valve requires 3 and 1/2, turns. Full closure of this valve would have prevented the start of the 3B main steam generator feedwater pump.
2) Valve 3-20-765 [SJ:ISV], high side isolation valve for the main steam generator feedwater pump suction strainer differential pressure [SJ:PDS] was found closed instead of open. The as found condition of this valve would not have prevented the closure of the supply breaker to the 3B main steam generator feedwater pump.

Each of these valves had been recently verified to be in their required position.

The cause for the mispositioned valves is indeterminate.

IV. ANALYSIS OF THE EVENT The loss of normal feedwater flow, is an analyzed event in the Updated Final Safety Analysis Report (UFSAR)(Section 14.1.11.1).

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'ACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY POINT UNIT 3 05000250 97-004-00 4 OF 5 Following is a discussion of that analysis. A loss of normal feedwater results in a reduction in capability of the secondary system to remove heat generated in the reactor core. In the case of this event the reactor was in Mode 3 and had not started up since the shutdown for refueling on March 3, 1997. Therefore the heat in the core was limited to the remaining decay heat of the core and the heat generated by the running reactor coolant pumps.

If an alternate supply of feedwater were not supplied to the plant, core residual heat could cause a primary system heatup.

The residual heat in this event was minimal compared to the analyzed event.

Three turbine driven auxiliary feedwater pumps start on the trip of all main feedwater pumps to supply feedwater to the s""am generators for continued heat removal from the reactor coolant system.

The assumptions in the UFSAR accident analysis include initially operating at 102 % reactor power with reactor coolant at 6 degrees Fahrenheit higher than nominal, and a reactor trip occurring on low-,low steam generator water level. All of these assumptions would result in more residual heat than that present in the event which is the subject of this Licensee Event Report.

Analysis is presented in'he UFSAR to show that following a loss of normal feedwater, the auxiliary feedwater system is capable of removing the stored and residual heat, thus preventing either over pressurization of the reactor coolant system, over pressurization of the secondary side, or uncovery of the reactor core. Consequently, for the analyzed accident, the plant is able to return to a safe condition. In this event no unsafe condition existed.

Since the plant was tripped in Mode 3, and the steam generator heat transfer capability was not reduced, the primary system variables never approached a departure from nucleate boiling condition.

Based on the above, the health "nd safety of the public were not adversely affected.

V. CORRECTIVE ACTIONS

1) The valves listed as inappropriately positioned were repositioned.

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'ACIL'ITY NAME DOCKET NUMBER LER NUMBER PAGE NO.

TURKEY POINT UNIT 3 05000250 97-004-00 5OF5

2) Starting alternatives to avoid auxiliary feedwater initiation upon failure of an initial main steam generator feedwater pump start will be evaluated.
3) Procedure O-SMI-059.2, "Outside Containment Instrument Independent Verification Inspection," will be revised to include more explicit direction on how to ensure listed instruments are in service. This corrective action applies to both Units 3 and 4.
4) Individuals responsible for verification of proper alignment of valves prior to pump operation were counseled.

VI. ADDITIONAL INFORMATION EIIS "odes are shown in the format [EIIS SYSTEM: IEEE component function identifier, second component function identifier (if appropriate)j.

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