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{{Adams|number = ML101170629}}
{{Adams
| number = ML101170629
| issue date = 04/27/2010
| title = IR 05000341-10-002; on 01/01/2010 - 03/31/2010; Fermi Power Plant, Unit 2; Routine Integrated Inspection Report
| author name = Giessner J
| author affiliation = NRC/RGN-III/DRP/B4
| addressee name = Davis J
| addressee affiliation = Detroit Edison
| docket = 05000341
| license number = NPF-043
| contact person =
| case reference number = FOIA/PA-2010-0209
| document report number = IR-10-002
| document type = Inspection Report, Letter
| page count = 38
}}


{{IR-Nav| site = 05000341 | year = 2010 | report number = 002 }}
{{IR-Nav| site = 05000341 | year = 2010 | report number = 002 }}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:ril 27, 2010
[[Issue date::April 27, 2010]]


Mr. Jack Senior Vice President and Chief Nuclear Officer Detroit Edison Company Fermi 2 - 210 NOC 6400 North Dixie Highway Newport, MI 48166
==SUBJECT:==
FERMI POWER PLANT, UNIT 2, INTEGRATED INSPECTION REPORT 05000341/2010002


SUBJECT: FERMI POWER PLANT, UNIT 2, INTEGRATED INSPECTION REPORT 05000341/2010002
==Dear Mr. Davis:==
On March 31, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection findings, which were discussed on April 12, 2010, with J. Plona and other members of your staff.
 
The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


==Dear Mr. Davis:==
Based on the results of this inspection, a licensee-identified violation, which was determined to be of very low safety significance, is described in Section 40A7 of this report.
On March 31, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection findings, which were discussed on April 12, 2010, with J. Plona and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commission's rules and regulations and with the conditions of your license.


The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, a licensee-identified violation, which was determined to be of very low safety significance, is described in Section 40A7 of this report. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/ John B. Giessner, Chief Branch 4 Division of Reactor Projects Docket No. 50-341 License No. NPF-43  
Sincerely,
/RA/
John B. Giessner, Chief Branch 4 Division of Reactor Projects Docket No. 50-341 License No. NPF-43


===Enclosure:===
===Enclosure:===
Inspection Report 05000341/2010002
Inspection Report 05000341/2010002 w/Attachment: Supplemental Information


===w/Attachment:===
REGION III==
Supplemental Information
Docket No: 50-341 License No: NPF-43 Report No: 05000341/2010002 Licensee: Detroit Edison Company Facility: Fermi Power Plant, Unit 2 Location: Newport, MI Dates: January 1 through March 31, 2010 Inspectors: R. Morris, Senior Resident Inspector R. Jones, Resident Inspector M. Learn, DNMS Reactor Engineer M. Mitchell, Health Physicist F. Tran, Reactor Engineer Approved by: J. Giessner, Chief Branch 4 Division of Reactor Projects Enclosure
 
=SUMMARY OF FINDINGS=
Inspection Report (IR) 05000341/2010002; 01/01/2010 - 03/31/2010; Fermi Power Plant,


cc w/encl: Distribution via ListServ
Unit 2; routine integrated report. This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.


Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket No: 50-341 License No: NPF-43 Report No: 05000341/2010002 Licensee: Detroit Edison Company Facility: Fermi Power Plant, Unit 2 Location: Newport, MI Dates: January 1 through March 31, 2010 Inspectors: R. Morris, Senior Resident Inspector R. Jones, Resident Inspector M. Learn, DNMS Reactor Engineer M. Mitchell, Health Physicist F. Tran, Reactor Engineer Approved by: J. Giessner, Chief Branch 4 Division of Reactor Projects
===NRC-Identified===
and Self-Revealed Findings No findings of significance were identified.


Enclosure
===Licensee-Identified Violations===


=SUMMARY OF FINDINGS=
A violation of very low safety significance identified by the licensee has been reviewed by inspectors. Corrective actions planned or taken by the licensee have been entered into the licensees corrective action program. This violation and corrective action tracking numbers are listed in Section 4OA7 of this report.
...........................................................................................................1


=REPORT DETAILS=
=REPORT DETAILS=
.......................................................................................................................2 Summary of Plant Status...........................................................................................................2
 
===Summary of Plant Status===
 
Fermi Unit 2 started this inspection period at 100 percent power and remained there until March 5, 2010, when power was reduced to 62 percent in preparation to repair the A reactor recirculation motor generator (RRMG) set speed controller. Due to an increase in offgas flow, the power was increased to 100 percent on March 6 to stabilize offgas flow. On March 22, power was reduced to 50 percent to repair the scoop tube controller for the A RRMG set. On March 25, a power increase was commenced and the main generator tripped on a differential relay signal. The main generator trip actuated a main turbine trip and a subsequent reactor scram. The plant was started on March 30 and returned to 100 percent power on March


==REACTOR SAFETY==
==REACTOR SAFETY==
.......................................................................................................2
 
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity===
{{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
{{IP sample|IP=IP 71111.01}}
...............................................................2
===.1 Readiness for Impending Adverse Weather Condition - Heavy Snowfall Conditions===
{{a|1R04}}
 
====a. Inspection Scope====
On January 7, 2010, a winter weather advisory was issued for expected snow squalls.
 
The inspectors observed the licensees preparations and planning for the significant winter weather potential. The inspectors reviewed licensee procedures and discussed potential compensatory measures with control room personnel. The inspectors focused on plant managements actions for implementing the stations procedures for ensuring adequate personnel for safe plant operation and emergency response would be available. The inspectors conducted a site walkdown including walkdowns of various plant structures and systems to check for maintenance or other apparent deficiencies that could affect system operations during the predicted significant weather. The inspectors also reviewed corrective action program (CAP) items to verify the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Specific documents reviewed during this inspection are listed in the Attachment.
 
This inspection constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure (IP) 71111.01-05.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Readiness of Offsite and Alternate AC Power Systems===
 
====a. Inspection Scope====
The inspectors verified that plant features and procedures for operation and continued availability of offsite and alternate AC power systems during adverse weather were appropriate. The inspectors reviewed the licensees procedures affecting these areas and the communications protocols between the transmission system operator (TSO) and the plant to verify the appropriate information was being exchanged when issues arose that could impact the offsite power system. Examples of aspects considered in the inspectors review included:
* coordination between the TSO and the plant during off-normal or emergency events;
* explanations for the events;
* estimates of when the offsite power system would be returned to a normal state; and
* notifications from the TSO to the plant when the offsite power system was returned to normal.
 
The inspectors also verified that plant procedures addressed measures to monitor and maintain availability and reliability of both the offsite AC power system and the onsite alternate AC power system prior to or during adverse weather conditions. Specifically, the inspectors verified the procedures addressed the following:
* actions to be taken when notified by the TSO that the post-trip voltage of the offsite power system at the plant would not be acceptable to assure the continued operation of the safety-related loads without transferring to the onsite power supply;
* compensatory actions identified to be performed if it would not be possible to predict the post-trip voltage at the plant for the current grid conditions;
* re-assessment of plant risk based on maintenance activities which could affect grid reliability, or the ability of the transmission system to provide offsite power; and
* communications between the plant and the TSO when changes at the plant could impact the transmission system, or when the capability of the transmission system to provide adequate offsite power was challenged.
 
The inspectors also reviewed CAP items to verify the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one readiness of offsite and alternate AC power systems sample as defined in IP 71111.01-05.
 
====b. Findings====
No findings of significance were identified {{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
..........................................................................4
===.1 Quarterly Partial System Walkdowns===
{{a|1R05}}
 
====a. Inspection Scope====
The inspectors performed partial system walkdowns of the following risk-significant systems:
* Non-isolatable instrument air system division 1;
* Division 1 and division 2 core spray; and
* Combustion turbine generator 11-1 electrical and fuel system.
 
The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders(WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify there were no obvious deficiencies. The inspectors also verified the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment.
 
These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
.....................................................................................4
===.1 Routine Resident Inspector Tours===
{{a|1R11}}
{{IP sample|IP=IP 71111.05Q}}
 
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
* Turbine building basement, north end;
* Reactor building, fourth floor, RRMG set room;
* Reactor building, third floor, east side and standby liquid control;
* Auxiliary building, third floor, reactor protection system (RPS) motor generator(MG) sets and DC motor control center area;
* Personnel air lock, first floor; and
* Control room overhead, fourth floor.
 
The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; fire detectors and sprinklers were unobstructed; transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP. Documents reviewed are listed in the to this report.
 
These activities constituted six quarterly fire protection inspection samples as defined in IP 71111.05-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R11}}
==1R11 Licensed Operator Requalification Program==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
{{IP sample|IP=IP 71111.11}}
.......................................5
===.1 Resident Inspector Quarterly Review===
{{a|1R12}}
{{IP sample|IP=IP 71111.11Q}}
 
====a. Inspection Scope====
On February 9, 2010, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
* licensed operator performance;
* crews clarity and formality of communications;
* ability to take timely actions in the conservative direction;
* prioritization, interpretation, and verification of annunciator alarms;
* correct use and implementation of abnormal and emergency procedures;
* control board manipulations;
* oversight and direction from supervisors; and
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.
 
The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.
 
====b. Findings====
No findings of significance were identified. {{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}
.................................................................6
===.1 Routine Quarterly Evaluations===
{{a|1R13}}
{{IP sample|IP=IP 71111.12Q}}
 
====a. Inspection Scope====
The inspectors evaluated degraded performance issues involving the following risk-significant systems:
* Emergency diesel generators (EDGs); and
* Standby gas treatment system.
 
The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
* implementing appropriate work practices;
* identifying and addressing common cause failures;
* scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
* characterizing system reliability issues for performance;
* charging unavailability for performance;
* trending key parameters for condition monitoring;
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
* verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).
 
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two quarterly maintenance effectiveness samples as defined in IP 71111.12-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
............7
===.1 Maintenance Risk Assessments and Emergent Work Control===
{{a|1R15}}
 
====a. Inspection Scope====
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify the appropriate risk assessments were performed prior to removing equipment for work:
* Risk during downpower with failed relay on Number 3 High Pressure Stop Valve;
* Risk during EDG-13 safety system outage, half turbine trip, and loss of turbine building heating, ventilating, and air conditioning (HVAC);
* Risk during turbine building loss of HVAC and RRMG set lube oil pump vibration increase;
* Risk during condenser vacuum leak, Turbine Building Closed Cooling Water Motor trip; and
* Risk during trip of A RRMG set on startup.
 
These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
 
These maintenance risk assessments and emergent work control activities constituted five samples as defined in IP 71111.13-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R15}}
==1R15 Operability Evaluations==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}
.......................................................................7
===.1 Operability Evaluations===
{{a|1R18}}
 
====a. Inspection Scope====
The inspectors reviewed the following issues:
* CARD 09-29116; Increase in main generator slip ring end air side hydrogen seal oil flow;
* CARD 09-29290; ODMI 09-015 off-gas increase flow;
* CARD 10-20556; EFA-R32-10-003 revision of DC-0367 Volume 1 predicts operation of residual heat removal (low pressure coolant injection) above rated motor horsepower;
* CARD 10-21733; Configuration Design Basis Inspection (CDBI) DC-0919 load tap changer and motor starting; and
* UFSAR Change 16, Section 9.1.4.2; Fuel Handling System Equipment Design.
 
The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.
 
This operability inspection constituted five samples as defined in IP 71111.15-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R18}}
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}
..............................................................................8
===.1 Temporary Plant Modifications===
{{a|1R19}}
 
====a. Inspection Scope====
The inspectors reviewed the following temporary modification (TM):
* TM 2010-0003; Main Turbine Low Pressure Exhaust Hood Temperature Trip Switch.
 
The inspectors compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TS, as applicable, to verify the modification did not affect the operability or availability of the affected system(s). The inspectors also compared the licensees information to operating experience information to ensure lessons learned from other utilities had been incorporated into the licensees decision to implement the temporary modification. The inspectors, as applicable, performed field verifications to ensure the modifications were installed as directed; the modifications operated as expected; modification testing adequately demonstrated continued system operability, availability, and reliability; and operation of the modifications did not impact the operability of any interfacing systems. Lastly, the inspectors discussed the temporary modification with operations, engineering, and training personnel to ensure the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance. Documents reviewed in the course of this inspection are listed in the to this report.
 
This inspection constituted one temporary modification sample as defined in IP 71111.18-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R19}}
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
..................................................................9
===.1 Post-Maintenance Testing===
{{a|1R22}}
 
====a. Inspection Scope====
The inspectors reviewed the following post-maintenance activities to verify procedures and test activities were adequate to ensure system operability and functional capability:
* WO 30823085; Number 3 HPSV RPS relay failed to reset;
* WO D198060100: EDG 13 post-maintenance testing (PMT) following safety system outage;
* Reactor core isolation cooling (RCIC) standard operating procedure run after maintenance;
* WO 30966771; Turbine Building HVAC supply fan used and exhaust fan;
* Division 2 Control Center HVAC pressure control switch calibration after failure to control;
* Condenser vacuum leak repairs and downpower PMT; and
* WO 30618215; RRMG set A scoop tube locked.
 
These activities were selected based upon the SSCs ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure the test results adequately ensured the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with PMTs to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted seven PMT samples as defined in IP 71111.19-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R22}}
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}
..........................................................................10
===.1 Surveillance Testing===
 
====a. Inspection Scope====
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
* Inspection and testing of multi-contact auxiliary relays, C71A-19D (routine);
* Procedure 24.110.05; RPS Turbine Control and Stop Valve Functional Test (routine);
* Procedure 24.206.01; RCIC Pump and Valve Test (in-service testing);
* Procedure 24.413.03; Division 2 Control Room Emergency Filter Monthly Operability Test (routine);
* Procedure 42.302.12; 4160 Bus 65F Undervoltage Circulation Calibration and Functional Surveillance (routine);
* Procedure 44.030.251; Emergency Core Cooling System Reactor Vessel Water Level (Level 1, 2, & 8) Division 1, Channel A Functional Test, and Procedure 44.030.253, Channel C (routine); and
* WO 26910317; Perform 24.307.47 EDG 13 Fast Start Followed by Load Reject (routine).
 
The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:
* did preconditioning occur;
* were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
* were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
* plant equipment calibration was correct, accurate, and properly documented;
* as-left setpoints were within required ranges; and the calibration frequency was in accordance with TSs, the USAR, procedures, and applicable commitments;
* measuring and test equipment calibration was current;
* test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
* test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
* test data and results were accurate, complete, within limits, and valid;
* test equipment was removed after testing;
* where applicable for in-service testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the system design basis;
* where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
* where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
* where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
* prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
* equipment was returned to a position or status required to support the performance of its safety functions; and
* all problems identified during the testing were appropriately documented and dispositioned in the CAP.
 
Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted six routine surveillance testing samples and one in-service testing sample as defined in IP 71111.22, Sections -02 and -05.
 
====b. Findings====
No findings of significance were identified.


==RADIATION SAFETY==
==RADIATION SAFETY==
...................................................................................................11 2PS1 Radioactive Gaseous and Liquid Effluent Treatment (IP71124.06)....................11
2PS1 Radioactive Gaseous and Liquid Effluent Treatment (IP71124.06)      This inspection constituted one sample as defined in IP 71124.06-05.
{{a|2RS0}}
 
==2RS0 7 Rogical Environmental Monitoring Program and Radioactive Material Control     Program==
===.1 Inspection Planning and Program Reviews (02.01)===
{{IP sample|IP=IP 71124.07}}
 
............................................................................................17
Event Report and Effluent Report Reviews
 
====a. Inspection Scope====
The inspectors reviewed the Radiological Effluent Release Reports issued since the last inspection to determine if the reports were submitted as required by the Offsite Dose Calculation Manual (ODCM)/Radiological Environmental Technical Specifications (RETS). The inspectors reviewed anomalous results, unexpected trends, or abnormal releases identified by the licensee for further inspection to determine if they were evaluated, were entered in the CAP, and were adequately resolved.
 
The inspectors identified radioactive effluent monitor operability issues reported by the licensee as provided in effluent release reports, to review these issues during the onsite inspection, as warranted, given their relative significance and determine if the issues were entered into the CAP and adequately resolved.
 
====b. Findings====
No findings of significance were identified.
Offsite Dose Calculation Manual and Final Safety Analysis Report Review
 
====a. Inspection Scope====
The inspectors reviewed Final Safety Analysis Report (UFSAR) descriptions of the radioactive effluent monitoring systems, treatment systems, and effluent flow paths so they could be verified during inspection walkdowns. The inspectors reviewed changes to the ODCM made by the licensee since the last inspection against the guidance in NUREG-1301, 1302 and 0133, and Regulatory Guides 1.109, 1.21 and 4.1.
 
When differences were identified, the inspectors reviewed the technical basis or evaluations of the change during the onsite inspection, to determine whether they were technically justified and maintain effluent releases as-low-as-is-reasonably-achievable (ALARA).
 
The inspectors reviewed licensee documentation to determine if the licensee has identified any non-radioactive systems that have become contaminated as disclosed either through an event report or the ODCM since the last inspection. This review provided an intelligent sample list for the onsite inspection of any 10 CFR 50.59 evaluations and allowed a determination if any newly contaminated systems have an unmonitored effluent discharge path to the environment, whether any required ODCM revisions were made to incorporate these new pathways and whether the associated effluents were reported in accordance with Regulatory Guide 1.21.
 
====b. Findings====
No findings of significance were identified.
Groundwater Protection Initiative Program
 
====a. Inspection Scope====
The inspectors reviewed reported groundwater monitoring results and changes to the licensees written program for identifying and controlling contaminated spills/leaks to groundwater.
 
====b. Findings====
No findings of significance were identified.
Procedures, Special Reports, and Other Documents
 
====a. Inspection Scope====
The inspectors reviewed Licensee Event Reports, event reports, and/or special reports related to the effluent program issued since the previous inspection to identify any additional focus areas for the inspection based on the scope/breadth of problems described in these reports. The review included effluent program implementing procedures, particularly those associated with effluent sampling, effluent monitor set-point determinations, and dose calculations. The review also included copies of licensee and third-party (independent) evaluation reports of the effluent monitoring program since the last inspection to gather insights into the licensees program and aid in selecting areas for inspection review (smart sampling).
 
====b. Findings====
No findings of significance were identified.
 
===.2 Walkdowns and Observations (02.02)===
 
====a. Inspection Scope====
The inspectors walked down selected components of the gaseous and liquid discharge systems to verify that equipment configuration and flow paths align with the documents reviewed in Section 02.01 above and to assess equipment material condition. Special attention was made to identify potential unmonitored release points (such as open roof vents in boiling water reactors turbine decks, temporary structures butted against turbine, auxiliary or containment buildings), building alterations which could impact airborne, or liquid, effluent controls, and ventilation system leakage that communicates directly with the environment.
 
For equipment or areas associated with the systems selected for review that were not readily accessible due to radiological conditions, the inspectors reviewed the licensee's material condition surveillance records, as applicable.
 
The inspectors walked down those filtered ventilation systems whose test results were reviewed to verify that there are no conditions, such as degraded High Efficiency Particulate Air charcoal banks, improper alignment, or system installation issues that would impact the performance, or the effluent monitoring capability, of the effluent system.
 
The inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluent (including sample collection and analysis) to verify that appropriate treatment equipment was used and the processing activities align with discharge permits.
 
The inspectors assessed whether the licensee has made significant changes to their effluent release points (e.g., changes subject to a 10 CFR 50.59 review or require NRC approval of alternate discharge points).
 
The inspectors did not observe selected portions of the routine processing and discharge liquid waste (including sample collection and analysis) to verify that appropriate effluent treatment equipment is being used and that radioactive liquid waste is being processed and discharged in accordance with procedure requirements and aligns with discharge permits, because the licensee does not conduct discharge of liquid waste and has not done so since the mid-1990s.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Sampling and Analyses (02.03)===
 
====a. Inspection Scope====
The inspectors selected three effluent sampling activities, consistent with smart sampling, to verify that adequate controls have been implemented to ensure representative samples are obtained (e.g., provisions for sample line flushing, vessel recirculation, composite samplers, etc.).
The inspectors selected three effluent discharges made with inoperable (declared out-of-service) effluent radiation monitors to verify that controls are in place to ensure compensatory sampling is performed consistent with the RETS/ODCM and that those controls are adequate to prevent the release of unmonitored liquid and gaseous effluents.
 
The inspectors assessed whether the facility is routinely relying on the use of compensatory sampling in-lieu of adequate system maintenance, based on the frequency of compensatory sampling since the last inspection.
 
The inspectors reviewed the results of the inter-laboratory comparison program to assess the quality of the radioactive effluent sample analyses to verify that the inter-laboratory comparison program include hard-to-detect isotopes as appropriate.
 
====b. Findings====
No findings of significance were identified.
 
===.4 Instrumentation and Equipment (02.04)===
 
Effluent Flow Measuring Instruments
 
====a. Inspection Scope====
The inspectors reviewed the methodology the licensee uses to determine the effluent stack and vent flow rates to verify that the flow rates are consistent with RETS/ODCM or UFSAR values, and that differences between assumed and actual stack and vent flow rates do not affect the results of the projected public doses.
 
====b. Findings====
No findings of significance were identified.
Air Cleaning Systems
 
====a. Inspection Scope====
The inspectors evaluated whether surveillance test results since the previous inspection for TS required ventilation effluent discharge systems (HEPA and charcoal filtration),such as the standby gas treatment system (boiling water reactors), meet TS acceptance criteria.
 
====b. Findings====
No findings of significance were identified.
 
===.5 Dose Calculations (02.05)===
 
====a. Inspection Scope====
The inspectors reviewed all significant changes in reported dose values compared to the previous Radiological Effluent Release Report (e.g., a factor of 5, or increases that approach Appendix I Criteria) to evaluate the factors, which may have resulted in the change.
 
The inspectors reviewed three gaseous waste discharge permits to verify that the projected doses to members of the public were accurate and based on representative samples of the discharge path.
 
Inspectors evaluated the methods used to determine the isotopes that are included in the source term to ensure all applicable radionuclides are included, within detectability standards. The review included the current 10 CFR Part 61 analyses to ensure hard-to-detect radionuclides are included in the source term.
 
The inspectors reviewed changes in the licensees offsite dose calculations since the last inspection to verify the changes are consistent with the ODCM and Regulatory Guide 1.109. Inspectors reviewed meteorological dispersion and deposition factors used in the ODCM and effluent dose calculations to ensure appropriate factors are being used for public dose calculations.
 
The inspectors reviewed the latest Land Use Census to verify that changes (e.g.,
significant increases or decreases to population in the plant environs, changes in critical exposure pathways, the location of nearest member of the public or critical receptor, etc.) have been factored into the dose calculations.
 
For the releases reviewed above, the inspectors assessed whether the calculated doses (monthly, quarterly, and annual dose) are within the 10 CFR Part 50, Appendix I, and TS dose criteria.
 
The inspectors selected, as available, records of any abnormal gaseous or liquid tank discharges (e.g., discharges resulting from misaligned valves, valve leak-by, etc.) to ensure the abnormal discharge was monitored by the discharge point effluent monitor.
 
There were no abnormal discharges. Discharges made with inoperable effluent radiation monitors, or unmonitored leakages, were reviewed to ensure that an evaluation was made of the discharge to satisfy 10 CFR 20.1501 so as to account for the source term and projected doses to the public.
 
====b. Findings====
No findings of significance were identified.
 
===.6 Groundwater Protection Initiative Implementation (02.06)===
 
====a. Inspection Scope====
The inspectors assessed whether the licensee is continuing to implement the Voluntary Nuclear Energy Institute (NEI)/Industry Groundwater Protection Initiative (GPI) since the last inspection. The inspectors reviewed:
* monitoring results of the GPI to determine if the licensee has implemented its program as intended, and to identify any anomalous results (anomalous results or missed samples were reviewed to determine if the licensee has identified and addressed deficiencies through its CAP);
* identified leakage or spill events and entries made into 10 CFR 50.75
: (g) records to assess any remediation actions taken for effectiveness and onsite contamination events involving contamination of ground water to assess whether the source of the leak or spill was identified and mitigated; and
* unmonitored spills, leaks, or unexpected liquid or gaseous discharges, to ensure that an evaluation was performed to determine the type and amount of radioactive material that was discharged, assess whether sufficient radiological surveys were performed to evaluate the extent of the contamination and the radiological source term, and verify that a survey/evaluation had been performed to include consideration of hard-to-detect radionuclides.
 
The inspectors reviewed whether the licensee completed offsite notifications (State, local, and if appropriate, the NRC) as provided in its GPI implementing procedures.
 
The inspectors reviewed the evaluation of discharges from onsite surface water bodies (ponds, retention basins, lakes) that contain or potentially contain radioactivity, and the potential for ground water leakage from these onsite surface water bodies to determine if licensees are properly accounting for discharges from these surface water bodies as part of their effluent release reports.
 
The inspectors assessed whether onsite ground water sample results and a description of any significant onsite leaks/spills into ground water for each calendar year was documented in the Annual Radiological Environmental Operating Report for the Radiological Environmental Monitoring Program (REMP) or the Annual Radiological Effluent Release Report for the RETS. For significant, new effluent discharge points (such as significant or continuing leakage to ground water that continues to impact the environment if not remediated), the inspectors determined if the ODCM was updated to include any new release points.
 
====b. Findings====
No findings of significance were identified.
 
===.7 Problem Identification and Resolution (02.07)===
 
====a. Inspection Scope====
Inspectors evaluated whether problems associated with the effluent monitoring and control program are being identified by the licensee at an appropriate threshold and are properly addressed for resolution in the licensee CAP. In addition, they assessed appropriateness of the corrective actions for selected sample of problems documented by the licensee involving radiation monitoring and exposure controls.
 
====b. Findings====
No findings of significance were identified.
 
2RS07 Radiological Environmental Monitoring Program and Radioactive Material Control Program (71124.07)
This inspection constituted one sample as defined in IP 71124.07-05
 
===.1 Inspection Planning (02.01)===
 
====a. Inspection Scope====
The inspectors reviewed the annual radiological environmental operating reports and the results of any licensee assessments since the last inspection, to verify that the REMP was implemented in accordance with the TS and ODCM. This review included report changes to the ODCM with respect to environmental monitoring, commitments in terms of sampling locations, monitoring and measurement frequencies, land use census, inter-laboratory comparison program, and analysis of data.
 
The inspectors reviewed the ODCM to identify locations of environmental monitoring stations and the UFSAR for information regarding the environmental monitoring program and meteorological monitoring instrumentation.
 
The inspectors reviewed quality assurance audit results of the program to assist in choosing inspection smart samples and audits and technical evaluations performed on the vendor laboratory program.
 
The inspectors reviewed the annual effluent release report and the 10 CFR Part 61, Licensing Requirements for Land Disposal of Radioactive Waste, report to determine if the licensee is sampling, as appropriate, for the predominant and dose-causing radionuclides likely to be released in effluents.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Site Inspection (02.02)===
 
====a. Inspection Scope====
The inspectors walked down three of the air sampling stations and five of the thermoluminescent dosimeter (TLD) monitoring stations to determine whether they are located as described in the ODCM and to determine the equipment material condition.
 
Consistent with smart sampling, the air sampling stations were selected based on the locations with the highest X/Q, D/Q wind sectors, and TLDs were selected based on the most risk-significant locations (e.g., those that have the highest potential for public dose impact). For the air samplers and TLDs selected, the inspectors reviewed the calibration and maintenance records to verify that they demonstrate adequate operability of these components. Additionally, the review included the calibration and maintenance records of composite water samplers and evaluation to determine if the licensee has initiated sampling of other appropriate media upon loss of a required sampling station. The licensee does not use composite samplers.
 
The inspectors observed the collection and preparation of two environmental samples from different environmental media (e.g., ground and surface water, milk, vegetation, sediment, and soil) as available to verify that environmental sampling is representative of the release pathways as specified in the ODCM and that sampling techniques are in accordance with procedures.
 
By direct observation and review of records, the inspectors evaluated the meteorological instruments to verify they are operable, calibrated, and maintained in accordance with guidance contained in the UFSAR, NRC Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants, and licensee procedures. Also, the inspectors assessed whether the meteorological data readout and recording instruments in the control room and, if applicable, at the tower were operable.
 
The inspectors assessed whether missed and/or anomalous environmental samples are identified and reported in the annual environmental monitoring report. They selected five events that involved a missed sample, inoperable sampler, lost TLD, or anomalous measurement to verify that the licensee has identified the cause and has implemented corrective actions. The inspectors reviewed the licensees assessment of any positive sample results (i.e., licensed radioactive material detected above the lower limits of detection (LLDs)) and reviewed the associated radioactive effluent release data that was the source of the released material.
 
Inspectors selected three SSCs that involve or could reasonably involve licensed material for which there is a credible mechanism for licensed material to reach ground water, and evaluated whether the licensee has implemented a sampling and monitoring program sufficient to detect leakage of these SSCs to ground water.
 
The inspectors assessed whether records, as required by 10 CFR 50.75(g), of leaks, spills, and remediation since the previous inspection are retained in a retrievable manner.
 
The inspectors reviewed any significant changes made by the licensee to the ODCM as the result of changes to the land census, long-term meteorological conditions (3-year average), or modifications to the sampler stations since the last inspection. They reviewed technical justifications for any changed sampling locations to verify that the licensee performed the reviews required to ensure that the changes did not affect its ability to monitor the impacts of radioactive effluent releases on the environment.
 
The inspectors evaluated whether the appropriate detection sensitivities with respect to TS/ODCM are used for counting samples (i.e., the samples meet the TS/ODCM required LLDs). The inspectors reviewed the results of the vendors quality control program, including the inter-laboratory comparison program, to verify the adequacy of the environmental sample analyses vendor laboratory program, and to verify that the inter-laboratory comparison test including the media/nuclide mix was appropriate for the facility.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Identification and Resolution of Problems (02.03)===
 
====a. Inspection Scope====
The inspectors assessed whether problems associated with the REMP are being identified by the licensee at an appropriate threshold and are properly addressed for resolution in the licensees CAP. Additionally, they evaluated the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involved the REMP.
 
====b. Findings====
No findings of significance were identified.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
....................................................................................................19
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
.........................................................19
===.1 Unplanned Scrams per 7000 Critical Hours===
{{a|4OA2}}
 
====a. Inspection Scope====
The inspectors sampled licensee submittals for the unplanned scrams per 7000 critical hours performance indicator (PI) for the period from the first quarter 2009 through the fourth quarter 2009. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Revision 6 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, and NRC inspection reports for the period of January 1, 2009, through December 31, 2009, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment.
 
This inspection constituted one unplanned scram per 7000 critical hours sample as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Unplanned Scrams with Complications===
 
====a. Inspection Scope====
The inspectors sampled licensee submittals for the unplanned scrams with complications PI for the period from the first quarter 2009 through the fourth quarter 2009. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Revision 6 of the NEI Document 99-02 were used.
 
The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, and NRC integrated inspection reports for the period of January 1, 2008, through December 31, 2009, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment.
 
This inspection constituted one unplanned scram with complications sample as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Unplanned Transients per 7000 Critical Hours===
 
====a. Inspection Scope====
The inspectors sampled licensee submittals for the unplanned transients per 7000 critical hours PI for the period from the first quarter 2009 through the fourth quarter 2009.
 
To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports, and NRC integrated inspection reports for the period of January 2, 2008, through December 31, 2009. to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one unplanned transients per 7000 critical hours sample as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified. {{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
..............................................20
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
{{a|4OA3}}
 
===.1 Routine Review of Items Entered into the Corrective Action Program===
 
====a. Inspection Scope====
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees CAP at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent-of-condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the Attachment.
 
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Daily Corrective Action Program Reviews===
 
====a. Inspection Scope====
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily condition report packages.
 
These daily reviews were performed by procedure as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Selected Issue Follow-Up Inspection: In-Depth Apparent Cause Evaluation===
 
====a. Inspection Scope====
The inspectors selected the following action request for an in-depth review:
* In-Depth Apparent Cause Evaluation; CARD 09-29635, Mispositioned Component: Division 1 emergency equipment cooling water (EECW) makeup pump keylock switch was in OFF instead of AUTO as required by the standby lineup.
 
The inspectors discussed the evaluations and associated corrective actions with licensee personnel and verified the following attributes during their review of the above apparent cause evaluation:
* complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
* consideration of the extent of condition, generic implications, common cause, and previous occurrences;
* classification and prioritization of the resolution of the problem, commensurate with safety significance;
* identification of the contributing causes of the problem; and
* identification of corrective actions, which were appropriately focused to correct the problem.
 
The above constitutes completion of one in-depth problem identification and resolution sample as defined in IP 71152-05
 
====b. Findings====
No findings of significance were identified. {{a|4OA3}}
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
{{IP sample|IP=IP 71153}}
{{IP sample|IP=IP 71153}}
.................22
===.1 Main Condenser Inleakage during Planned Downpower===
{{a|4OA5}}
 
==4OA5 Other Activities....................................................................................................23 4OA6==
====a. Inspection Scope====
Management Meetings........................................................................................23 4OA7 Licensee-Identified Violations..............................................................................24
The inspectors reviewed the plants response to a planned downpower to repair RRMG set A. On March 5, 2010, the licensee performed a plant downpower to approximately 50 percent to perform repairs to the A RRMG set speed controller. During the downpower, the control room staff noted an increase in the offgas flow and subsequently the operators stopped the downpower at 62 percent. After several attempts to determine the source of the air in-leakage, the licensee decided to return power to 100 percent and stabilize the plant. As power increased, the offgas flow returned to a lower value and stabilized. The licensee prepared and performed a leak detection procedure. Upon completion of the repairs, the offgas flow was reduced to a value that allowed the plant to reduce power for repairs to the A RRMG set. Documents reviewed in this inspection are listed in the Attachment.
 
This event follow-up review constituted one sample as defined in IP 71153-05.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Reactor SCRAM during Power Ascension===
 
====a. Inspection Scope====
The inspectors reviewed the plants response to an automatic reactor shutdown due to a main turbine trip on March 25, 2010. At 2:27 p.m. on March 25, 2010, the reactor mode switch was taken to shutdown following an automatic scram due to a main turbine trip.
 
The scram was uncomplicated, and all control rods fully inserted into the core. The lowest reactor vessel water level reached was 136 inches; and as expected, high pressure coolant injection and RCIC did not actuate. Inspectors reviewed the licensee's reporting in accordance with 10 CFR 50.72. No safety relief valves actuated. The cause of the main turbine trip was determined on March 27, 2010, to be a ground on a current transformer on the main generator outlet. Documents reviewed in this inspection are listed in the Attachment.
 
This event follow-up review constituted one sample as defined in IP 71153-05.
 
====b. Findings====
No findings of significance were identified.
{{a|4OA5}}
==4OA5 Other Activities==
 
===.1 Preoperational and Operational Testing of an Independent Spent Fuel Storage===
 
Installation (60854.1)
 
====a. Inspection Scope====
An inspection of the licensees activities that support the implementation of an independent spent fuel storage installation at the Fermi Power Plant was initiated.
 
The inspection included in-office review of plant design calculations as well as on-site reviews of select dry run activities. Since preoperational testing of the licensee's ISFSI was still ongoing at the conclusion of this inspection period, this inspection did not constitute a sample as defined in IP 60854.1 and will be completed in the next routine quarterly inspection.
 
====b. Findings====
The results of this inspection will be documented in the next routine quarterly inspection.
{{a|4OA6}}
==4OA6 Management Meetings==
 
===.1 Exit Meeting Summary===
 
On April 12, 2010, the inspectors presented the inspection results to J. Plona, Site Vice-President, T. Conner, Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.
 
===.2 Interim Exit Meeting===
 
An interim exit meeting was conducted for:
* the Radiological Hazards Assessment and Exposure Control, Radioactive Gaseous and Liquid Effluent Treatment, Radiological Environmental Monitoring Program, and Radioactive Material Control Program inspection with the Director of Organizational Effectiveness, Ms. C. Walker, on March 26, 2010.
 
{{a|4OA7}}
==4OA7 Licensee-Identified Violations==
 
The following violation of very low significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
 
Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, states, in part, that Activities affecting quality shall be prescribed by documented procedures and shall be accomplished in accordance with these procedures. Contrary to the above, the licensee did not follow their approved procedures to place division 1 EECW makeup pump keylock control switch to AUTO before returning division 1 EECW to service. On December 15, 2009, in preparation for returning division 1 EECW to service, the licensee performed Procedure 23.127, Reactor Building Closed Cooling Water/EECW System, Section 5.10 and Attachment 4. The licensee also performed Procedure 24.207.08, Division 1 EECW Pump and Valve Operability Test, Section 5.1, and then returned the system to service at 5:01 a.m. EST on December 16, 2009. At 9:14 a.m., the licensee performed a quarterly surveillance test for the system using Procedure 24.207.08, Division 1 EECW Pump and Valve Operability Test, Section 5.2.
 
During performance of the surveillance test, the licensee discovered the P4400M058A, Division 1 EECW makeup pump keylock control switch, was in OFF instead of AUTO as expected. This condition had rendered Division 1 EECW inoperable and resulted in an unplanned entry into a 72-hour shutdown Limiting Condition for Operation. The licensee documented this issue in CARD 09-29635. Immediate corrective actions were to stop the quarterly surveillance test, to place the keylock control switch to AUTO, perform Procedure 23.127, Section 5.10, Standby Mode EECW Division 1, and perform Procedure 23.127, Attachment 4, Division 1 RBCCW/EECW Standby Verification Check List. The licensee determined the cause to be procedure adherence deficiencies. This finding was a violation of 10 CFR Part 50, Appendix B, Criterion V. Using the Significance Determination Process in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008, the inspectors determined the finding to be of very low safety significance because the issue did not result in the actual loss of a safety function.
 
Since the issue was of very low significance (Green) and was discovered during a normally scheduled surveillance, the issue is considered licensee identified.
 
ATTACHMENT:


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
==KEY POINTS OF CONTACT==
Licensee
: [[contact::J. Plona]], Fermi 2 Site Vice-President
: [[contact::T. Conner]], Plant Manager
: [[contact::M. Caragher]], Engineering Director
: [[contact::R. Johnson]], Licensing Manager
: [[contact::E. Kokosky]], Radiation Protection Manager
: [[contact::R. LaBurn]], Assistant Radiation Protection Manager
: [[contact::T. Lashley]], Radiological Engineer
: [[contact::T. VanderMey]], Principle Radiological Engineer
Nuclear Regulatory Commission
: [[contact::J. Giessner]], Branch 4
Attachment
==LIST OF DOCUMENTS REVIEWED==


}}
}}

Latest revision as of 19:13, 21 December 2019

IR 05000341-10-002; on 01/01/2010 - 03/31/2010; Fermi Power Plant, Unit 2; Routine Integrated Inspection Report
ML101170629
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 04/27/2010
From: Jack Giessner
Reactor Projects Region 3 Branch 4
To: Jennifer Davis
Detroit Edison
References
FOIA/PA-2010-0209 IR-10-002
Download: ML101170629 (38)


Text

ril 27, 2010

SUBJECT:

FERMI POWER PLANT, UNIT 2, INTEGRATED INSPECTION REPORT 05000341/2010002

Dear Mr. Davis:

On March 31, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection findings, which were discussed on April 12, 2010, with J. Plona and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, a licensee-identified violation, which was determined to be of very low safety significance, is described in Section 40A7 of this report.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

John B. Giessner, Chief Branch 4 Division of Reactor Projects Docket No. 50-341 License No. NPF-43

Enclosure:

Inspection Report 05000341/2010002 w/Attachment: Supplemental Information

REGION III==

Docket No: 50-341 License No: NPF-43 Report No: 05000341/2010002 Licensee: Detroit Edison Company Facility: Fermi Power Plant, Unit 2 Location: Newport, MI Dates: January 1 through March 31, 2010 Inspectors: R. Morris, Senior Resident Inspector R. Jones, Resident Inspector M. Learn, DNMS Reactor Engineer M. Mitchell, Health Physicist F. Tran, Reactor Engineer Approved by: J. Giessner, Chief Branch 4 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

Inspection Report (IR) 05000341/2010002; 01/01/2010 - 03/31/2010; Fermi Power Plant,

Unit 2; routine integrated report. This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified

and Self-Revealed Findings No findings of significance were identified.

Licensee-Identified Violations

A violation of very low safety significance identified by the licensee has been reviewed by inspectors. Corrective actions planned or taken by the licensee have been entered into the licensees corrective action program. This violation and corrective action tracking numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Fermi Unit 2 started this inspection period at 100 percent power and remained there until March 5, 2010, when power was reduced to 62 percent in preparation to repair the A reactor recirculation motor generator (RRMG) set speed controller. Due to an increase in offgas flow, the power was increased to 100 percent on March 6 to stabilize offgas flow. On March 22, power was reduced to 50 percent to repair the scoop tube controller for the A RRMG set. On March 25, a power increase was commenced and the main generator tripped on a differential relay signal. The main generator trip actuated a main turbine trip and a subsequent reactor scram. The plant was started on March 30 and returned to 100 percent power on March

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Readiness for Impending Adverse Weather Condition - Heavy Snowfall Conditions

a. Inspection Scope

On January 7, 2010, a winter weather advisory was issued for expected snow squalls.

The inspectors observed the licensees preparations and planning for the significant winter weather potential. The inspectors reviewed licensee procedures and discussed potential compensatory measures with control room personnel. The inspectors focused on plant managements actions for implementing the stations procedures for ensuring adequate personnel for safe plant operation and emergency response would be available. The inspectors conducted a site walkdown including walkdowns of various plant structures and systems to check for maintenance or other apparent deficiencies that could affect system operations during the predicted significant weather. The inspectors also reviewed corrective action program (CAP) items to verify the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Specific documents reviewed during this inspection are listed in the Attachment.

This inspection constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings of significance were identified.

.2 Readiness of Offsite and Alternate AC Power Systems

a. Inspection Scope

The inspectors verified that plant features and procedures for operation and continued availability of offsite and alternate AC power systems during adverse weather were appropriate. The inspectors reviewed the licensees procedures affecting these areas and the communications protocols between the transmission system operator (TSO) and the plant to verify the appropriate information was being exchanged when issues arose that could impact the offsite power system. Examples of aspects considered in the inspectors review included:

  • coordination between the TSO and the plant during off-normal or emergency events;
  • explanations for the events;
  • estimates of when the offsite power system would be returned to a normal state; and
  • notifications from the TSO to the plant when the offsite power system was returned to normal.

The inspectors also verified that plant procedures addressed measures to monitor and maintain availability and reliability of both the offsite AC power system and the onsite alternate AC power system prior to or during adverse weather conditions. Specifically, the inspectors verified the procedures addressed the following:

  • actions to be taken when notified by the TSO that the post-trip voltage of the offsite power system at the plant would not be acceptable to assure the continued operation of the safety-related loads without transferring to the onsite power supply;
  • compensatory actions identified to be performed if it would not be possible to predict the post-trip voltage at the plant for the current grid conditions;
  • re-assessment of plant risk based on maintenance activities which could affect grid reliability, or the ability of the transmission system to provide offsite power; and
  • communications between the plant and the TSO when changes at the plant could impact the transmission system, or when the capability of the transmission system to provide adequate offsite power was challenged.

The inspectors also reviewed CAP items to verify the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one readiness of offsite and alternate AC power systems sample as defined in IP 71111.01-05.

b. Findings

No findings of significance were identified

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • Non-isolatable instrument air system division 1;
  • Combustion turbine generator 11-1 electrical and fuel system.

The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders(WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify there were no obvious deficiencies. The inspectors also verified the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment.

These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

  • Turbine building basement, north end;
  • Reactor building, fourth floor, RRMG set room;
  • Personnel air lock, first floor; and
  • Control room overhead, fourth floor.

The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; fire detectors and sprinklers were unobstructed; transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP. Documents reviewed are listed in the to this report.

These activities constituted six quarterly fire protection inspection samples as defined in IP 71111.05-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On February 9, 2010, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk-significant systems:

The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly maintenance effectiveness samples as defined in IP 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify the appropriate risk assessments were performed prior to removing equipment for work:

  • Risk during downpower with failed relay on Number 3 High Pressure Stop Valve;
  • Risk during EDG-13 safety system outage, half turbine trip, and loss of turbine building heating, ventilating, and air conditioning (HVAC);
  • Risk during turbine building loss of HVAC and RRMG set lube oil pump vibration increase;
  • Risk during condenser vacuum leak, Turbine Building Closed Cooling Water Motor trip; and
  • Risk during trip of A RRMG set on startup.

These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted five samples as defined in IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • CARD 09-29116; Increase in main generator slip ring end air side hydrogen seal oil flow;
  • CARD 09-29290; ODMI 09-015 off-gas increase flow;
  • CARD 10-21733; Configuration Design Basis Inspection (CDBI) DC-0919 load tap changer and motor starting; and
  • UFSAR Change 16, Section 9.1.4.2; Fuel Handling System Equipment Design.

The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.

This operability inspection constituted five samples as defined in IP 71111.15-05.

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

.1 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the following temporary modification (TM):

  • TM 2010-0003; Main Turbine Low Pressure Exhaust Hood Temperature Trip Switch.

The inspectors compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TS, as applicable, to verify the modification did not affect the operability or availability of the affected system(s). The inspectors also compared the licensees information to operating experience information to ensure lessons learned from other utilities had been incorporated into the licensees decision to implement the temporary modification. The inspectors, as applicable, performed field verifications to ensure the modifications were installed as directed; the modifications operated as expected; modification testing adequately demonstrated continued system operability, availability, and reliability; and operation of the modifications did not impact the operability of any interfacing systems. Lastly, the inspectors discussed the temporary modification with operations, engineering, and training personnel to ensure the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance. Documents reviewed in the course of this inspection are listed in the to this report.

This inspection constituted one temporary modification sample as defined in IP 71111.18-05.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify procedures and test activities were adequate to ensure system operability and functional capability:

  • WO D198060100: EDG 13 post-maintenance testing (PMT) following safety system outage;
  • Division 2 Control Center HVAC pressure control switch calibration after failure to control;

These activities were selected based upon the SSCs ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure the test results adequately ensured the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with PMTs to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted seven PMT samples as defined in IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • Inspection and testing of multi-contact auxiliary relays, C71A-19D (routine);
  • Procedure 24.110.05; RPS Turbine Control and Stop Valve Functional Test (routine);
  • Procedure 24.206.01; RCIC Pump and Valve Test (in-service testing);
  • Procedure 24.413.03; Division 2 Control Room Emergency Filter Monthly Operability Test (routine);
  • Procedure 42.302.12; 4160 Bus 65F Undervoltage Circulation Calibration and Functional Surveillance (routine);
  • WO 26910317; Perform 24.307.47 EDG 13 Fast Start Followed by Load Reject (routine).

The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  • were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was in accordance with TSs, the USAR, procedures, and applicable commitments;
  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for in-service testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the system design basis;
  • where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
  • where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
  • where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
  • prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
  • equipment was returned to a position or status required to support the performance of its safety functions; and
  • all problems identified during the testing were appropriately documented and dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted six routine surveillance testing samples and one in-service testing sample as defined in IP 71111.22, Sections -02 and -05.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

2PS1 Radioactive Gaseous and Liquid Effluent Treatment (IP71124.06) This inspection constituted one sample as defined in IP 71124.06-05.

.1 Inspection Planning and Program Reviews (02.01)

Event Report and Effluent Report Reviews

a. Inspection Scope

The inspectors reviewed the Radiological Effluent Release Reports issued since the last inspection to determine if the reports were submitted as required by the Offsite Dose Calculation Manual (ODCM)/Radiological Environmental Technical Specifications (RETS). The inspectors reviewed anomalous results, unexpected trends, or abnormal releases identified by the licensee for further inspection to determine if they were evaluated, were entered in the CAP, and were adequately resolved.

The inspectors identified radioactive effluent monitor operability issues reported by the licensee as provided in effluent release reports, to review these issues during the onsite inspection, as warranted, given their relative significance and determine if the issues were entered into the CAP and adequately resolved.

b. Findings

No findings of significance were identified.

Offsite Dose Calculation Manual and Final Safety Analysis Report Review

a. Inspection Scope

The inspectors reviewed Final Safety Analysis Report (UFSAR) descriptions of the radioactive effluent monitoring systems, treatment systems, and effluent flow paths so they could be verified during inspection walkdowns. The inspectors reviewed changes to the ODCM made by the licensee since the last inspection against the guidance in NUREG-1301, 1302 and 0133, and Regulatory Guides 1.109, 1.21 and 4.1.

When differences were identified, the inspectors reviewed the technical basis or evaluations of the change during the onsite inspection, to determine whether they were technically justified and maintain effluent releases as-low-as-is-reasonably-achievable (ALARA).

The inspectors reviewed licensee documentation to determine if the licensee has identified any non-radioactive systems that have become contaminated as disclosed either through an event report or the ODCM since the last inspection. This review provided an intelligent sample list for the onsite inspection of any 10 CFR 50.59 evaluations and allowed a determination if any newly contaminated systems have an unmonitored effluent discharge path to the environment, whether any required ODCM revisions were made to incorporate these new pathways and whether the associated effluents were reported in accordance with Regulatory Guide 1.21.

b. Findings

No findings of significance were identified.

Groundwater Protection Initiative Program

a. Inspection Scope

The inspectors reviewed reported groundwater monitoring results and changes to the licensees written program for identifying and controlling contaminated spills/leaks to groundwater.

b. Findings

No findings of significance were identified.

Procedures, Special Reports, and Other Documents

a. Inspection Scope

The inspectors reviewed Licensee Event Reports, event reports, and/or special reports related to the effluent program issued since the previous inspection to identify any additional focus areas for the inspection based on the scope/breadth of problems described in these reports. The review included effluent program implementing procedures, particularly those associated with effluent sampling, effluent monitor set-point determinations, and dose calculations. The review also included copies of licensee and third-party (independent) evaluation reports of the effluent monitoring program since the last inspection to gather insights into the licensees program and aid in selecting areas for inspection review (smart sampling).

b. Findings

No findings of significance were identified.

.2 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors walked down selected components of the gaseous and liquid discharge systems to verify that equipment configuration and flow paths align with the documents reviewed in Section 02.01 above and to assess equipment material condition. Special attention was made to identify potential unmonitored release points (such as open roof vents in boiling water reactors turbine decks, temporary structures butted against turbine, auxiliary or containment buildings), building alterations which could impact airborne, or liquid, effluent controls, and ventilation system leakage that communicates directly with the environment.

For equipment or areas associated with the systems selected for review that were not readily accessible due to radiological conditions, the inspectors reviewed the licensee's material condition surveillance records, as applicable.

The inspectors walked down those filtered ventilation systems whose test results were reviewed to verify that there are no conditions, such as degraded High Efficiency Particulate Air charcoal banks, improper alignment, or system installation issues that would impact the performance, or the effluent monitoring capability, of the effluent system.

The inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluent (including sample collection and analysis) to verify that appropriate treatment equipment was used and the processing activities align with discharge permits.

The inspectors assessed whether the licensee has made significant changes to their effluent release points (e.g., changes subject to a 10 CFR 50.59 review or require NRC approval of alternate discharge points).

The inspectors did not observe selected portions of the routine processing and discharge liquid waste (including sample collection and analysis) to verify that appropriate effluent treatment equipment is being used and that radioactive liquid waste is being processed and discharged in accordance with procedure requirements and aligns with discharge permits, because the licensee does not conduct discharge of liquid waste and has not done so since the mid-1990s.

b. Findings

No findings of significance were identified.

.3 Sampling and Analyses (02.03)

a. Inspection Scope

The inspectors selected three effluent sampling activities, consistent with smart sampling, to verify that adequate controls have been implemented to ensure representative samples are obtained (e.g., provisions for sample line flushing, vessel recirculation, composite samplers, etc.).

The inspectors selected three effluent discharges made with inoperable (declared out-of-service) effluent radiation monitors to verify that controls are in place to ensure compensatory sampling is performed consistent with the RETS/ODCM and that those controls are adequate to prevent the release of unmonitored liquid and gaseous effluents.

The inspectors assessed whether the facility is routinely relying on the use of compensatory sampling in-lieu of adequate system maintenance, based on the frequency of compensatory sampling since the last inspection.

The inspectors reviewed the results of the inter-laboratory comparison program to assess the quality of the radioactive effluent sample analyses to verify that the inter-laboratory comparison program include hard-to-detect isotopes as appropriate.

b. Findings

No findings of significance were identified.

.4 Instrumentation and Equipment (02.04)

Effluent Flow Measuring Instruments

a. Inspection Scope

The inspectors reviewed the methodology the licensee uses to determine the effluent stack and vent flow rates to verify that the flow rates are consistent with RETS/ODCM or UFSAR values, and that differences between assumed and actual stack and vent flow rates do not affect the results of the projected public doses.

b. Findings

No findings of significance were identified.

Air Cleaning Systems

a. Inspection Scope

The inspectors evaluated whether surveillance test results since the previous inspection for TS required ventilation effluent discharge systems (HEPA and charcoal filtration),such as the standby gas treatment system (boiling water reactors), meet TS acceptance criteria.

b. Findings

No findings of significance were identified.

.5 Dose Calculations (02.05)

a. Inspection Scope

The inspectors reviewed all significant changes in reported dose values compared to the previous Radiological Effluent Release Report (e.g., a factor of 5, or increases that approach Appendix I Criteria) to evaluate the factors, which may have resulted in the change.

The inspectors reviewed three gaseous waste discharge permits to verify that the projected doses to members of the public were accurate and based on representative samples of the discharge path.

Inspectors evaluated the methods used to determine the isotopes that are included in the source term to ensure all applicable radionuclides are included, within detectability standards. The review included the current 10 CFR Part 61 analyses to ensure hard-to-detect radionuclides are included in the source term.

The inspectors reviewed changes in the licensees offsite dose calculations since the last inspection to verify the changes are consistent with the ODCM and Regulatory Guide 1.109. Inspectors reviewed meteorological dispersion and deposition factors used in the ODCM and effluent dose calculations to ensure appropriate factors are being used for public dose calculations.

The inspectors reviewed the latest Land Use Census to verify that changes (e.g.,

significant increases or decreases to population in the plant environs, changes in critical exposure pathways, the location of nearest member of the public or critical receptor, etc.) have been factored into the dose calculations.

For the releases reviewed above, the inspectors assessed whether the calculated doses (monthly, quarterly, and annual dose) are within the 10 CFR Part 50, Appendix I, and TS dose criteria.

The inspectors selected, as available, records of any abnormal gaseous or liquid tank discharges (e.g., discharges resulting from misaligned valves, valve leak-by, etc.) to ensure the abnormal discharge was monitored by the discharge point effluent monitor.

There were no abnormal discharges. Discharges made with inoperable effluent radiation monitors, or unmonitored leakages, were reviewed to ensure that an evaluation was made of the discharge to satisfy 10 CFR 20.1501 so as to account for the source term and projected doses to the public.

b. Findings

No findings of significance were identified.

.6 Groundwater Protection Initiative Implementation (02.06)

a. Inspection Scope

The inspectors assessed whether the licensee is continuing to implement the Voluntary Nuclear Energy Institute (NEI)/Industry Groundwater Protection Initiative (GPI) since the last inspection. The inspectors reviewed:

  • monitoring results of the GPI to determine if the licensee has implemented its program as intended, and to identify any anomalous results (anomalous results or missed samples were reviewed to determine if the licensee has identified and addressed deficiencies through its CAP);
  • identified leakage or spill events and entries made into 10 CFR 50.75
(g) records to assess any remediation actions taken for effectiveness and onsite contamination events involving contamination of ground water to assess whether the source of the leak or spill was identified and mitigated; and
  • unmonitored spills, leaks, or unexpected liquid or gaseous discharges, to ensure that an evaluation was performed to determine the type and amount of radioactive material that was discharged, assess whether sufficient radiological surveys were performed to evaluate the extent of the contamination and the radiological source term, and verify that a survey/evaluation had been performed to include consideration of hard-to-detect radionuclides.

The inspectors reviewed whether the licensee completed offsite notifications (State, local, and if appropriate, the NRC) as provided in its GPI implementing procedures.

The inspectors reviewed the evaluation of discharges from onsite surface water bodies (ponds, retention basins, lakes) that contain or potentially contain radioactivity, and the potential for ground water leakage from these onsite surface water bodies to determine if licensees are properly accounting for discharges from these surface water bodies as part of their effluent release reports.

The inspectors assessed whether onsite ground water sample results and a description of any significant onsite leaks/spills into ground water for each calendar year was documented in the Annual Radiological Environmental Operating Report for the Radiological Environmental Monitoring Program (REMP) or the Annual Radiological Effluent Release Report for the RETS. For significant, new effluent discharge points (such as significant or continuing leakage to ground water that continues to impact the environment if not remediated), the inspectors determined if the ODCM was updated to include any new release points.

b. Findings

No findings of significance were identified.

.7 Problem Identification and Resolution (02.07)

a. Inspection Scope

Inspectors evaluated whether problems associated with the effluent monitoring and control program are being identified by the licensee at an appropriate threshold and are properly addressed for resolution in the licensee CAP. In addition, they assessed appropriateness of the corrective actions for selected sample of problems documented by the licensee involving radiation monitoring and exposure controls.

b. Findings

No findings of significance were identified.

2RS07 Radiological Environmental Monitoring Program and Radioactive Material Control Program (71124.07)

This inspection constituted one sample as defined in IP 71124.07-05

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the annual radiological environmental operating reports and the results of any licensee assessments since the last inspection, to verify that the REMP was implemented in accordance with the TS and ODCM. This review included report changes to the ODCM with respect to environmental monitoring, commitments in terms of sampling locations, monitoring and measurement frequencies, land use census, inter-laboratory comparison program, and analysis of data.

The inspectors reviewed the ODCM to identify locations of environmental monitoring stations and the UFSAR for information regarding the environmental monitoring program and meteorological monitoring instrumentation.

The inspectors reviewed quality assurance audit results of the program to assist in choosing inspection smart samples and audits and technical evaluations performed on the vendor laboratory program.

The inspectors reviewed the annual effluent release report and the 10 CFR Part 61, Licensing Requirements for Land Disposal of Radioactive Waste, report to determine if the licensee is sampling, as appropriate, for the predominant and dose-causing radionuclides likely to be released in effluents.

b. Findings

No findings of significance were identified.

.2 Site Inspection (02.02)

a. Inspection Scope

The inspectors walked down three of the air sampling stations and five of the thermoluminescent dosimeter (TLD) monitoring stations to determine whether they are located as described in the ODCM and to determine the equipment material condition.

Consistent with smart sampling, the air sampling stations were selected based on the locations with the highest X/Q, D/Q wind sectors, and TLDs were selected based on the most risk-significant locations (e.g., those that have the highest potential for public dose impact). For the air samplers and TLDs selected, the inspectors reviewed the calibration and maintenance records to verify that they demonstrate adequate operability of these components. Additionally, the review included the calibration and maintenance records of composite water samplers and evaluation to determine if the licensee has initiated sampling of other appropriate media upon loss of a required sampling station. The licensee does not use composite samplers.

The inspectors observed the collection and preparation of two environmental samples from different environmental media (e.g., ground and surface water, milk, vegetation, sediment, and soil) as available to verify that environmental sampling is representative of the release pathways as specified in the ODCM and that sampling techniques are in accordance with procedures.

By direct observation and review of records, the inspectors evaluated the meteorological instruments to verify they are operable, calibrated, and maintained in accordance with guidance contained in the UFSAR, NRC Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants, and licensee procedures. Also, the inspectors assessed whether the meteorological data readout and recording instruments in the control room and, if applicable, at the tower were operable.

The inspectors assessed whether missed and/or anomalous environmental samples are identified and reported in the annual environmental monitoring report. They selected five events that involved a missed sample, inoperable sampler, lost TLD, or anomalous measurement to verify that the licensee has identified the cause and has implemented corrective actions. The inspectors reviewed the licensees assessment of any positive sample results (i.e., licensed radioactive material detected above the lower limits of detection (LLDs)) and reviewed the associated radioactive effluent release data that was the source of the released material.

Inspectors selected three SSCs that involve or could reasonably involve licensed material for which there is a credible mechanism for licensed material to reach ground water, and evaluated whether the licensee has implemented a sampling and monitoring program sufficient to detect leakage of these SSCs to ground water.

The inspectors assessed whether records, as required by 10 CFR 50.75(g), of leaks, spills, and remediation since the previous inspection are retained in a retrievable manner.

The inspectors reviewed any significant changes made by the licensee to the ODCM as the result of changes to the land census, long-term meteorological conditions (3-year average), or modifications to the sampler stations since the last inspection. They reviewed technical justifications for any changed sampling locations to verify that the licensee performed the reviews required to ensure that the changes did not affect its ability to monitor the impacts of radioactive effluent releases on the environment.

The inspectors evaluated whether the appropriate detection sensitivities with respect to TS/ODCM are used for counting samples (i.e., the samples meet the TS/ODCM required LLDs). The inspectors reviewed the results of the vendors quality control program, including the inter-laboratory comparison program, to verify the adequacy of the environmental sample analyses vendor laboratory program, and to verify that the inter-laboratory comparison test including the media/nuclide mix was appropriate for the facility.

b. Findings

No findings of significance were identified.

.3 Identification and Resolution of Problems (02.03)

a. Inspection Scope

The inspectors assessed whether problems associated with the REMP are being identified by the licensee at an appropriate threshold and are properly addressed for resolution in the licensees CAP. Additionally, they evaluated the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involved the REMP.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Unplanned Scrams per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the unplanned scrams per 7000 critical hours performance indicator (PI) for the period from the first quarter 2009 through the fourth quarter 2009. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Revision 6 of the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, and NRC inspection reports for the period of January 1, 2009, through December 31, 2009, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment.

This inspection constituted one unplanned scram per 7000 critical hours sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Unplanned Scrams with Complications

a. Inspection Scope

The inspectors sampled licensee submittals for the unplanned scrams with complications PI for the period from the first quarter 2009 through the fourth quarter 2009. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Revision 6 of the NEI Document 99-02 were used.

The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, and NRC integrated inspection reports for the period of January 1, 2008, through December 31, 2009, to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Attachment.

This inspection constituted one unplanned scram with complications sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.3 Unplanned Transients per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the unplanned transients per 7000 critical hours PI for the period from the first quarter 2009 through the fourth quarter 2009.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports, and NRC integrated inspection reports for the period of January 2, 2008, through December 31, 2009. to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one unplanned transients per 7000 critical hours sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees CAP at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent-of-condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the Attachment.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings of significance were identified.

.3 Selected Issue Follow-Up Inspection: In-Depth Apparent Cause Evaluation

a. Inspection Scope

The inspectors selected the following action request for an in-depth review:

  • In-Depth Apparent Cause Evaluation; CARD 09-29635, Mispositioned Component: Division 1 emergency equipment cooling water (EECW) makeup pump keylock switch was in OFF instead of AUTO as required by the standby lineup.

The inspectors discussed the evaluations and associated corrective actions with licensee personnel and verified the following attributes during their review of the above apparent cause evaluation:

  • complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
  • consideration of the extent of condition, generic implications, common cause, and previous occurrences;
  • classification and prioritization of the resolution of the problem, commensurate with safety significance;
  • identification of the contributing causes of the problem; and
  • identification of corrective actions, which were appropriately focused to correct the problem.

The above constitutes completion of one in-depth problem identification and resolution sample as defined in IP 71152-05

b. Findings

No findings of significance were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 Main Condenser Inleakage during Planned Downpower

a. Inspection Scope

The inspectors reviewed the plants response to a planned downpower to repair RRMG set A. On March 5, 2010, the licensee performed a plant downpower to approximately 50 percent to perform repairs to the A RRMG set speed controller. During the downpower, the control room staff noted an increase in the offgas flow and subsequently the operators stopped the downpower at 62 percent. After several attempts to determine the source of the air in-leakage, the licensee decided to return power to 100 percent and stabilize the plant. As power increased, the offgas flow returned to a lower value and stabilized. The licensee prepared and performed a leak detection procedure. Upon completion of the repairs, the offgas flow was reduced to a value that allowed the plant to reduce power for repairs to the A RRMG set. Documents reviewed in this inspection are listed in the Attachment.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

No findings of significance were identified.

.2 Reactor SCRAM during Power Ascension

a. Inspection Scope

The inspectors reviewed the plants response to an automatic reactor shutdown due to a main turbine trip on March 25, 2010. At 2:27 p.m. on March 25, 2010, the reactor mode switch was taken to shutdown following an automatic scram due to a main turbine trip.

The scram was uncomplicated, and all control rods fully inserted into the core. The lowest reactor vessel water level reached was 136 inches; and as expected, high pressure coolant injection and RCIC did not actuate. Inspectors reviewed the licensee's reporting in accordance with 10 CFR 50.72. No safety relief valves actuated. The cause of the main turbine trip was determined on March 27, 2010, to be a ground on a current transformer on the main generator outlet. Documents reviewed in this inspection are listed in the Attachment.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 Preoperational and Operational Testing of an Independent Spent Fuel Storage

Installation (60854.1)

a. Inspection Scope

An inspection of the licensees activities that support the implementation of an independent spent fuel storage installation at the Fermi Power Plant was initiated.

The inspection included in-office review of plant design calculations as well as on-site reviews of select dry run activities. Since preoperational testing of the licensee's ISFSI was still ongoing at the conclusion of this inspection period, this inspection did not constitute a sample as defined in IP 60854.1 and will be completed in the next routine quarterly inspection.

b. Findings

The results of this inspection will be documented in the next routine quarterly inspection.

4OA6 Management Meetings

.1 Exit Meeting Summary

On April 12, 2010, the inspectors presented the inspection results to J. Plona, Site Vice-President, T. Conner, Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

.2 Interim Exit Meeting

An interim exit meeting was conducted for:

  • the Radiological Hazards Assessment and Exposure Control, Radioactive Gaseous and Liquid Effluent Treatment, Radiological Environmental Monitoring Program, and Radioactive Material Control Program inspection with the Director of Organizational Effectiveness, Ms. C. Walker, on March 26, 2010.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, states, in part, that Activities affecting quality shall be prescribed by documented procedures and shall be accomplished in accordance with these procedures. Contrary to the above, the licensee did not follow their approved procedures to place division 1 EECW makeup pump keylock control switch to AUTO before returning division 1 EECW to service. On December 15, 2009, in preparation for returning division 1 EECW to service, the licensee performed Procedure 23.127, Reactor Building Closed Cooling Water/EECW System, Section 5.10 and Attachment 4. The licensee also performed Procedure 24.207.08, Division 1 EECW Pump and Valve Operability Test, Section 5.1, and then returned the system to service at 5:01 a.m. EST on December 16, 2009. At 9:14 a.m., the licensee performed a quarterly surveillance test for the system using Procedure 24.207.08, Division 1 EECW Pump and Valve Operability Test, Section 5.2.

During performance of the surveillance test, the licensee discovered the P4400M058A, Division 1 EECW makeup pump keylock control switch, was in OFF instead of AUTO as expected. This condition had rendered Division 1 EECW inoperable and resulted in an unplanned entry into a 72-hour shutdown Limiting Condition for Operation. The licensee documented this issue in CARD 09-29635. Immediate corrective actions were to stop the quarterly surveillance test, to place the keylock control switch to AUTO, perform Procedure 23.127, Section 5.10, Standby Mode EECW Division 1, and perform Procedure 23.127, Attachment 4, Division 1 RBCCW/EECW Standby Verification Check List. The licensee determined the cause to be procedure adherence deficiencies. This finding was a violation of 10 CFR Part 50, Appendix B, Criterion V. Using the Significance Determination Process in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008, the inspectors determined the finding to be of very low safety significance because the issue did not result in the actual loss of a safety function.

Since the issue was of very low significance (Green) and was discovered during a normally scheduled surveillance, the issue is considered licensee identified.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

J. Plona, Fermi 2 Site Vice-President
T. Conner, Plant Manager
M. Caragher, Engineering Director
R. Johnson, Licensing Manager
E. Kokosky, Radiation Protection Manager
R. LaBurn, Assistant Radiation Protection Manager
T. Lashley, Radiological Engineer
T. VanderMey, Principle Radiological Engineer

Nuclear Regulatory Commission

J. Giessner, Branch 4

Attachment

LIST OF DOCUMENTS REVIEWED