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| | issue date = 06/04/1998 | | | issue date = 06/04/1998 |
| | title = LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr | | | title = LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr |
| | author name = DAHLBERG K A, WARD K D | | | author name = Dahlberg K, Ward K |
| | author affiliation = NIAGARA MOHAWK POWER CORP. | | | author affiliation = NIAGARA MOHAWK POWER CORP. |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:NIAGARA MOHAWK G EN ERATION BUSINESS GROUP NINE MILE POINT NUCLEAR STATION/lAKE ROAD, P.O.BOX 63, LYCOMING, NEW YORK 13093 dune 4, 1998'NNP2L 1788 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE: Docket No.50-410 LER 98-04, Supplement 1 Gentlemen: | | {{#Wiki_filter:NIAGARA MOHAWK G EN ERATION NINE MILE POINT NUCLEAR STATION/lAKEROAD, P.O. BOX 63, LYCOMING, NEW YORK 13093 BUSINESS GROUP dune 4, 1998 |
| In accordance with 10CFR50.73 (a)(2)(i)(B), we are submitting LER 98-04, Supplement 1,"Missed Technical Specification Required LSFT of Level 8 Trip of Main Turbine." This supplement is to clarify actions taken to correct the cause of knowledge deficiency. | | 'NNP2L 1788 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE: Docket No. 50-410 LER 98-04, Supplement 1 Gentlemen: |
| Very truly yours, Kim A.Dahlberg, Plant Manager-NhG?2 KAD/GJG/kap Attachment xc: Mr.H.J.Miller, Regional Administrator, Region I Mr.B.S.Norris, Senior Resident Inspector Records Management 9806ihoi40 50004ie PDR ADQCK 0 S 0 | | In accordance with 10CFR50.73 (a)(2)(i)(B), we are submitting LER 98-04, Supplement 1, "Missed Technical Specification Required LSFT of Level 8 Trip of Main Turbine." This supplement is to clarify actions taken to correct the cause of knowledge deficiency. |
| REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)ROVED OMB NO;3!500lcl EXPIRES: ESfJMATKD BURDEN PER RESPONSE TO COMPLY Wml Tl BS INFORMATION COLLECIION REQUESf c 50AJ HRS.FORWARD COMMENIS REGARDOIO BURDEN ESAMATK TO TIES RECORDS AND REPORTS MAN AGEMENf BRANCJ I (M30), U.S.NUCLEAR REGULATORY COMM lSS ION, WAS)BNGION, DC 3M55, AND TO THE PAPERWORK REDUCIION PROJECT O1500104), OFF)CHOP MANAGEMENf AND BUDGBI;WASHINGION, DC 30503 FACK1IY NAME (I)Nine Mile Point Unit 2 DOCXEf NUMBER (D 05000410 PAGE O)1 OF 4 TIILE (4)Missed Technical Specification Required LSFT of Level 8 Trip of Main Turbine EVENI'ATE (5)MONIH DAY*YEAR gag REVISION NUMBER REPORT DATEG)MONBl DAY YEAR OTHER FACILmES INVLVED (I)FACJLIIY NAMES 03 02 98 98 0 1 06 04 98 N/A N/A 05000 05000 OPERATING MODB (9)TIES REPORT IS SUBMIITIXI PURSUANT TO THK REQUIREMENIS OF IO CFR 5: (CJ>cca c>>c c>cc>>c>cc c/dscfcJJ>>wJ>>I)(I I)POWER LEVEL (lc)J>YK~>~W 0 20.2201(b) 0 20.2203(a)(1) 0 20.2203(a)(2)Q 0 20.2203(a)(2)(ii) 0 20.2203(a)(2)(iii) 0 20.2203(a)(2)(iv) 0 20.2203(a)(2)(v) 0 20.2203(a)(3) | | Very truly yours, Kim A. Dahlberg, Plant Manager - NhG?2 KAD/GJG/kap Attachment xc: Mr. H. J. Miller, Regional Administrator, Region I Mr. B. S. Norris, Senior Resident Inspector Records Management 9806ihoi40 0 50004ie PDR ADQCK S |
| Q 0 20.2203(a)(3)(ii) 0 20.2203(a)(4) 0 50.36(c)(1) 0 50.36(c)(2) 3 50.73(a)(2)Q 0 50.73(a)(2)(ii) 0$0.73(a)(2)(iii) 0$0.73(a)(2)(v) 0 50.73(a)(2)(v) 0 50.73(a)(2)(vii) 0 50.73(a)(2)(viii) 0 50.73(a)(2)(x) 073.7i 0 orHHt J>CccU>I>c>Ilcc>occ aclo>>>ccc>J J>c roc, J>BC Fcc>>c 555U NAME K.D.Ward-Technical Support Manager LICENSEE CONfACf FORTIES LKR (l1).TKIZPHONB NUMBER (315)349-1043 COMPLEIK ONB ISNB FOR EACH COMPONENf FAILURE DESCRIBED IN TIES REPORT (I3)REPORTABLB TO NPRDS SUPPLKMKNFAL REPORT EXPECIKD 0O 0 YES Q'ycc, co>tpkcc ZXFECIKD S Jtul5SJOJVJMIF>J 5 EXPIATED SUBMISSION DATE (l5)MONIH DAY ABSTRACT ghsltco140cPc>ccc>ac> | | |
| FFccc(>>~JJcj(/Jcasc0>IJccN>cc~
| | 0 REGULATORY COMMISSION ROVED OMB NO; 3!500lcl EXPIRES: |
| JJ>>cc)06)On March 2, 1998, Niagara Mohawk Power Corporation (NMPC)determined that the Nine Mile Point Unit 2 (MMP2)Logic System Functional Tests (LSFT)for the main turbine trip on high reactor vessel level (Level 8)failed to verify the entire circuit.This is a violation of Technical Specification Surveillance Requirement (TS SR)4.3.9.2 which is required to be performed at least once per 18 months.The cause of this event has been determined to be an apparent knowledge deficiency of the Electro Hydraulic Control (EHC)system combined with poor work practices, which led the LSFT procedure developers to conclude that the EHC panel was the actuated device.Contributing to this event was the omission of relevant information when the LSFT procedure for the Level 8 turbine trip was developed.
| | ESfJMATKD BURDEN PER RESPONSE TO COMPLY Wml TlBS INFORMATIONCOLLECIION LICENSEE EVENT REPORT (LER) REQUESf c 50AJ HRS. FORWARD COMMENIS REGARDOIO BURDEN ESAMATKTO TIES RECORDS AND REPORTS MANAGEMENfBRANCJ I (M30), U.S. NUCLEAR REGULATORY COMMlSS ION, WAS) BNGION, DC 3M55, ANDTO THE PAPERWORK REDUCIION PROJECT O1500104), OFF)CHOP MANAGEMENfAND BUDGBI; WASHINGION, DC 30503 FACK1IYNAME (I) DOCXEf NUMBER (D PAGE O) |
| The circuit diagrams for the Level 8 turbine trip show the EHC panel as a circuit termination.
| | Nine Mile Point Unit 2 05000410 1 OF 4 TIILE (4) |
| The applicable LSFT procedures will be revised prior to refueling outage 6 (RFO6).This event has been discussed with personnel performing the Generic Letter 96-01 procedure reviews. | | Missed Technical Specification Required LSFT of Level 8 Trip of Main Turbine EVENI'ATE(5) REPORT DATEG) OTHER FACILmES INVLVED(I) |
| 0 NRC FORM 366A FACILIIY NAME (I)REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION PROVED OMB NO.3)30010l EXPIRES: ESIIMATED BURDEN PER RESPONSE TO COMPLY Wml Tl IIS DIFORMATION COLLECfION REQUEST: SOA)I BLS.FORWARD COMMEÃfS REGARDBIG BURDEN ESIIMATE TO TIIE RECORDS AND REMRTS MANAGEMENI'RANCII (M30), US.NUCLEAR REGULATORY COMMISSION WASIENGfON>> | | MONIH DAY* YEAR gag REVISION MONBl DAY YEAR FACJLIIYNAMES NUMBER 03 02 98 98 0 1 06 04 98 N/A 05000 N/A 05000 OPERATING MODB (9) TIES REPORT IS SUBMIITIXIPURSUANT TO THK REQUIREMENIS OF IO CFR 5: (CJ>cca c>>c c>cc>>c>cc c/dscfcJJ>>wJ>>I) (II) |
| DC 3OSSSt AND TO THE PAPERWORK REDUCflON PROJECf OISOOIOQ, OFHCE OF MANAGEMENI'ND BUDGEf, WASIIINGTON, DC 20303.PAGE O)Nine Mile Point Unit 2 05000410 YEAR$98 04 REVISION NUMBER 0 1 02 OF 04 TE)ff Qnsarv tPtttt lt ttyket, sr@ofdMasd NRC iona SSSI's)P D On March 2, 1998, Niagara Mohawk Power Corporation (NMPC)determined that the Nine Mile Point Unit 2 (NMP2)Logic System Functional Tests (LSFT)for the main turbine trip on high reactor vessel level (Level 8)failed to verify the entire circuit.This is a violation of Technical Specification Surveillance Requirement (TS SR)4.3.9.2 which is required to be performed at least once per 18 months.This deficiency was identified in response to a question from another licensee concerning LSFT testing of the Electro Hydraulic Control (EHC)system.The EHC system engineer reviewed the LSFT drawings and determined that the EHC circuit had been tested from the Level 8 transmitter to an EHC panel in accordance with an LSFT procedure which references TS 4.3.9.2.The circuitry from the master trip bus within the EHC panel to the turbine stop and control valves was tested in accordance with an Instrument and Control surveillance procedure which did not specifically reference TS 4.3.9.2.However, the circuitry from the EHC panel input terminals to the master trip bus was not tested in either of the LSFT procedures. | | POWER LEVEL (lc) 0 20.2201(b) 0 20.2203(a)(2)(v) 3 50.73(a)(2)Q 0 50.73(a)(2)(viii) 0 20.2203(a)(1) 0 20.2203(a)(3) Q 0 50.73(a)(2)(ii) 0 50.73(a)(2)(x) 0 20.2203(a)(2)Q 0 20.2203(a)(3)(ii) 0 $ 0.73(a)(2)(iii) 073.7i 0 20.2203(a)(2)(ii) 0 20.2203(a)(4) 0 $ 0.73(a)(2)(v) 0 orHHt 0 20.2203(a)(2)(iii) 0 50.36(c)(1) 0 50.73(a)(2)(v) J>CccU> I>c >Ilcc>occ aclo>>> ccc>J Fcc>>c 555U J>c roc, J>BC J>YK~>~W 0 20.2203(a)(2)(iv) 0 50.36(c)(2) 0 50.73(a)(2)(vii) |
| After further review, it was found that the EHC panel circuitry from the input terminals to the master trip bus has been tested since Refueling Outage 3 in October 1993, but not by an LSFT.Work orders have been initiated with step text to perform the testing each refueling outage since RFO3.Therefore, the entire circuit has been tested since October 1993 to meet the LSFT requirements. | | LICENSEE CONfACf FORTIES LKR (l1) . |
| NMPC had performed two previous LSFT reviews and an initial review of this Level 8 LSFT as part of the overall LSFT review for Generic Letter (GL)96-01.None of these reviews identified this deficiency. | | NAME TKIZPHONB NUMBER K. D. Ward - Technical Support Manager (315) 349-1043 COMPLEIKONB ISNB FOR EACH COMPONENf FAILURE DESCRIBED IN TIES REPORT (I3) |
| However, the NhP2 GL 96-01 process has not been completed. | | REPORTABLB TO NPRDS SUPPLKMKNFALREPORT EXPECIKD 0O EXPIATED MONIH DAY SUBMISSION DATE (l5) 0 YES Q'ycc, co>tpkcc ZXFECIKDS Jtul5SJOJVJMIF>J 5 ABSTRACT ghsltco140cPc>ccc>ac> FFccc(>>~JJcj(/Jcasc0>IJccN>cc~ JJ>>cc) 06) |
| A senior engineer is required to perform an independent verification of the initial reviewer's work.That verification would likely have identified this deficiency. | | On March 2, 1998, Niagara Mohawk Power Corporation (NMPC) determined that the Nine Mile Point Unit 2 (MMP2) Logic System Functional Tests (LSFT) for the main turbine trip on high reactor vessel level (Level 8) failed to verify the entire circuit. This is a violation of Technical Specification Surveillance Requirement (TS SR) 4.3.9.2 which is required to be performed at least once per 18 months. |
| The cause of this event has been determined to be an apparent knowledge deficiency of the EHC system combined with poor work practices, which led the LSFT procedure developers to conclude that the EHC panel was the actuated device.Contributing to this event,was the omission of relevant information when the LSFT procedure for the Level 8 turbine trip was developed. | | The cause of this event has been determined to be an apparent knowledge deficiency of the Electro Hydraulic Control (EHC) system combined with poor work practices, which led the LSFT procedure developers to conclude that the EHC panel was the actuated device. Contributing to this event was the omission of relevant information when the LSFT procedure for the Level 8 turbine trip was developed. The circuit diagrams for the Level 8 turbine trip show the EHC panel as a circuit termination. |
| The circuit diagrams for the Level 8 turbine trip show the EHC panel as a circuit termination. | | The applicable LSFT procedures will be revised prior to refueling outage 6 (RFO6). This event has been discussed with personnel performing the Generic Letter 96-01 procedure reviews. |
| The cause of the individual not finding this during the initial GL 96-01 review was again knowledge deficiency and poor work practice.The individual believed that since the EHC/Turbine System is non-safety related, the actual trip of the main turbine was simply an economic issue to prevent turbine damage and not for reactor safety.Based on this, the individual did not pursue his review beyond the EHC panel input. | | |
| | 0 NRC FORM 366A REGULATORY COMMISSION PROVED OMB NO. 3)30010l EXPIRES: |
| | ESIIMATEDBURDEN PER RESPONSE TO COMPLY WmlTl IIS DIFORMATIONCOLLECfION LICENSEE EVENT REPORT (LER) REQUEST: SOA) IBLS. FORWARD COMMEÃfS REGARDBIG BURDEN ESIIMATETO TIIE TEXT CONTINUATION RECORDS AND REMRTS MANAGEMENI'RANCII(M30), US. NUCLEAR REGULATORY COMMISSION WASIENGfON>> DC 3OSSSt ANDTO THE PAPERWORK REDUCflON PROJECf OISOOIOQ, OFHCE OF MANAGEMENI'NDBUDGEf, WASIIINGTON,DC 20303. |
| | FACILIIYNAME(I) PAGE O) |
| | YEAR REVISION |
| | $ NUMBER Nine Mile Point Unit 2 05000410 98 04 0 1 02 OF 04 TE)ff Qnsarv tPtttt lt ttyket, sr@ ofdMasd NRC iona SSSI's) P D On March 2, 1998, Niagara Mohawk Power Corporation (NMPC) determined that the Nine Mile Point Unit 2 (NMP2) Logic System Functional Tests (LSFT) for the main turbine trip on high reactor vessel level (Level 8) failed to verify the entire circuit. This is a violation of Technical Specification Surveillance Requirement (TS SR) 4.3.9.2 which is required to be performed at least once per 18 months. |
| | This deficiency was identified in response to a question from another licensee concerning LSFT testing of the Electro Hydraulic Control (EHC) system. The EHC system engineer reviewed the LSFT drawings and determined that the EHC circuit had been tested from the Level 8 transmitter to an EHC panel in accordance with an LSFT procedure which references TS 4.3.9.2. The circuitry from the master trip bus within the EHC panel to the turbine stop and control valves was tested in accordance with an Instrument and Control surveillance procedure which did not specifically reference TS 4.3.9.2. However, the circuitry from the EHC panel input terminals to the master trip bus was not tested in either of the LSFT procedures. |
| | After further review, it was found that the EHC panel circuitry from the input terminals to the master trip bus has been tested since Refueling Outage 3 in October 1993, but not by an LSFT. Work orders have been initiated with step text to perform the testing each refueling outage since RFO3. Therefore, the entire circuit has been tested since October 1993 to meet the LSFT requirements. |
| | NMPC had performed two previous LSFT reviews and an initial review of this Level 8 LSFT as part of the overall LSFT review for Generic Letter (GL) 96-01. None of these reviews identified this deficiency. |
| | However, the NhP2 GL 96-01 process has not been completed. A senior engineer is required to perform an independent verification of the initial reviewer's work. That verification would likely have identified this deficiency. |
| | The cause of this event has been determined to be an apparent knowledge deficiency of the EHC system combined with poor work practices, which led the LSFT procedure developers to conclude that the EHC panel was the actuated device. Contributing to this event,was the omission of relevant information when the LSFT procedure for the Level 8 turbine trip was developed. The circuit diagrams for the Level 8 turbine trip show the EHC panel as a circuit termination. |
| | The cause of the individual not finding this during the initial GL 96-01 review was again knowledge deficiency and poor work practice. The individual believed that since the EHC/Turbine System is non-safety related, the actual trip of the main turbine was simply an economic issue to prevent turbine damage and not for reactor safety. Based on this, the individual did not pursue his review beyond the EHC panel input. |
| | |
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| NRC FORM 30SA REGULATORY COMMLSSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION PROVED OMB NO.31100I0(EXPIRES: ESTIMATED BURDEN PER RESPONSB TO COMPLY WIB I Tl BS INFORMATION COLLKCIION RE(IUESF: SOA)HRS.FORWARD COMMENTS REGARDB(G BURDEN ESIIMATETO THE RECORDS AND REPORTS MANAGEMKNI'RANCH (P>>030), UA.~REGULATORY COMMISSION, WASI BNQION>>DC 30SSS, AND TO TIIE PAPERWORK REDUCIION PROJKCP (IIS00104)>> | | NRC FORM 30SA REGULATORY COMMLSSION PROVED OMB NO. 31100I0( |
| OFFICE OP MANAGEMENI AND BUDGET>>WASIBNGION>> | | ~ |
| DC 30S03.FACLIIY NAME (I)LKR NUMBER (6)SEQUENIIAL NUMBER REVISION NUMBER PAGE(3)Nine Mile Point Unit 2 05000410 98 04 0 1 03 OF 04 TEXT Q'~apace 4 reqafraf, me ok5danaf NRC F~30'~'s)(II)This event is reportable in accordance with 10CFR50.73(a)(2)(i)(B),"any operation or condition prohibited by the plant's Technical Specifications." The purpose of the turbine trip on high water level is to cause a reactor scram to limit the minimum critical power ratio.NMP2 Updated Safety Analysis Report (USAR)Section 15.1.2, Feedwater Controller Failure-Maximum Demand, Subsection 15.1.2.2.3, Effect of Single Failures and Operator Errors, states"In Table 15.1-3, the first sensed event to initiate corrective action to the transient is the vessel high water level (L8)trip.Multiple level sensors are used to sense and detect when the water level reaches the L8 setpoint.At this point in the logic, a single failure will not initiate or prevent a turbine trip signal.Turbine trip signal transmission, however, is not built to single-failure criterion. | | EXPIRES: |
| The result of a failure at this point would have the effect of delaying the pressurization"signature." However, high moisture levels entering the turbine will be detected by high levels in the turbine s moisture separators, resulting in a trip of the unit." In addition, excessive moisture entering the turbine will cause vibration to the point where it too will trip the unit." Based upon these other turbine trip signals and associated reactor scram, the impact of not having this Level 8 trip is negligible. | | ESTIMATED BURDEN PER RESPONSB TO COMPLY WIBITlBS INFORMATIONCOLLKCIION LICENSEE EVENT REPORT (LER) RE(IUESF: SOA) HRS. FORWARD COMMENTS REGARDB(G BURDEN ESIIMATETOTHE TEXT CONTINUATION RECORDS AND REPORTS MANAGEMKNI'RANCH(P>>030), UA. REGULATORY COMMISSION, WASIBNQION>> DC 30SSS, ANDTO TIIE PAPERWORK REDUCIION PROJKCP (IIS00104)>> OFFICE OP MANAGEMENIAND BUDGET>> WASIBNGION>> DC 30S03. |
| Therefore, this event did not pose a threat to public health and safety or to plant personnel. | | FACLIIYNAME (I) LKR NUMBER (6) PAGE(3) |
| The applicable LSFT procedures will be revised prior to next use.2.This event has been reviewed and expectations reinforced with the personnel performing the GL 96-01 procedure reviews.The purpose of this review was to assure that personnel clearly understand that an LSFT is required to test from initiating device to the actuated device.The verification process for GL 96-01 will specifically address the LSFT circuit scope as part of the verification review.The verification reviews are scheduled for completion by the end of RFO6.Since the personnel who originally developed the EHC-LSFT procedures are no longer employed at NMPC, and Corrective Action 2 assured a thorough review, no additional training is warranted. | | SEQUENIIAL REVISION NUMBER NUMBER Nine Mile Point Unit 2 05000410 98 04 0 1 03 OF 04 TEXT Q'~ apace 4 reqafraf, me ok5danaf NRC F~ 30' 's) (II) |
| | This event is reportable in accordance with 10CFR50.73(a)(2)(i)(B), "any operation or condition prohibited by the plant's Technical Specifications." |
| | The purpose of the turbine trip on high water level is to cause a reactor scram to limit the minimum critical power ratio. NMP2 Updated Safety Analysis Report (USAR) Section 15.1.2, Feedwater Controller Failure-Maximum Demand, Subsection 15.1.2.2.3, Effect of Single Failures and Operator Errors, states "In Table 15.1-3, the first sensed event to initiate corrective action to the transient is the vessel high water level (L8) trip. Multiple level sensors are used to sense and detect when the water level reaches the L8 setpoint. At this point in the logic, a single failure will not initiate or prevent a turbine trip signal. Turbine trip signal transmission, however, is not built to single-failure criterion. The result of a failure at this point would have the effect of delaying the pressurization "signature." However, high moisture levels entering the turbine will be detected by high levels in the turbine s moisture separators, resulting in a trip of the unit." In addition, excessive moisture entering the turbine will cause vibration to the point where it too will trip the unit." |
| | Based upon these other turbine trip signals and associated reactor scram, the impact of not having this Level 8 trip is negligible. Therefore, this event did not pose a threat to public health and safety or to plant personnel. |
| | The applicable LSFT procedures willbe revised prior to next use. |
| | : 2. This event has been reviewed and expectations reinforced with the personnel performing the GL 96-01 procedure reviews. The purpose of this review was to assure that personnel clearly understand that an LSFT is required to test from initiating device to the actuated device. |
| | The verification process for GL 96-01 willspecifically address the LSFT circuit scope as part of the verification review. The verification reviews are scheduled for completion by the end of RFO6. |
| | Since the personnel who originally developed the EHC-LSFT procedures are no longer employed at NMPC, and Corrective Action 2 assured a thorough review, no additional training is warranted. |
| | |
| )) | | )) |
| FACLrrY NAME (I)UA.REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION PROVED OMB NO, 3 I 300104 EXPIRES: ESrMATED BURDEN PER RESPONSE TO COMPLY Wm(T)BS B(FORMATION COLLECIION REQUEST: 50A)HRS.FORWARD COMMENTS REGARDE(G BURDEN ESBMATE To THE RECORDS AND REPORTS M ANAGEM ENr BRANCH (M30), US.NUCLEAR REGULATORY COMMISSION WASHINGPON>>
| | UA. REGULATORY COMMISSION PROVED OMB NO, 3 I 300104 EXPIRES: |
| DC 30535>>AND To TIIB PAPERWORK REDUCIION PROJECI (3 I$00104)>>OFFICE OF MANAGEMENr AND BUDGEr>>WASKNGPON>> | | ESrMATED BURDEN PER RESPONSE TO COMPLY Wm( T)BS B(FORMATION COLLECIION LICENSEE EVENT REPORT (LER) REQUEST: 50A) HRS. FORWARD COMMENTS REGARDE(G BURDEN ESBMATE To THE TEXT CONTINUATION RECORDS AND REPORTS MANAGEMENr BRANCH (M30), US. NUCLEAR REGULATORY COMMISSION WASHINGPON>> DC 30535>> AND To TIIBPAPERWORK REDUCIION PROJECI (3 I $ 00104)>> OFFICE OF MANAGEMENrAND BUDGEr>> WASKNGPON>> DC 20503 FACLrrYNAME (I) PAGB O) |
| DC 20503 PAGB O)Nine Mile Point Unit 2 05000410 98 SEQUENfIAL NUMBER 04 REVISION NUMBER 0 1 04 OF 04 TExT Q'score 4F>>>>c!4 v te>>p(>>ef, are okbfaad hRc Fme 3!Is('sJ p D V.A.Failed components: | | SEQUENfIAL REVISION NUMBER NUMBER Nine Mile Point Unit 2 05000410 98 04 0 1 04 OF 04 TExT Q'score 4F>>>>c!4 v te>>p(>>ef, are okbfaad hRc Fme 3!Is('sJ p D V. |
| none.B.Previous similar events: NMP2 has had a number of instances where procedure preparation or review caused missed or inadequately performed surveillance tests.In accordance with NMPC's Corrective Action Program, a Deviation/Event Report (DER)was initiated to evaluate this trend.A root cause team was assembled to evaluate this overall trend to determine if process problems or other common aspects could be identified. | | A. Failed components: none. |
| Required corrective actions will be taken as necessary to correct any identified deficiencies in accordance with the corrective action program.C.IdentiGcation of components referred to in this LER: g>>??(?0?i',.",R>>S4>>(r0! | | B. Previous similar events: |
| I?+>>@>>>>?p I??li?~@"~'>>?)0 Pt~'qg F'P~'R??>>'>>>>??)?f??I'9? | | NMP2 has had a number of instances where procedure preparation or review caused missed or inadequately performed surveillance tests. In accordance with NMPC's Corrective Action Program, a Deviation/Event Report (DER) was initiated to evaluate this trend. A root cause team was assembled to evaluate this overall trend to determine ifprocess problems or other common aspects could be identified. Required corrective actions willbe taken as necessary to correct any identified deficiencies in accordance with the corrective action program. |
| ~Api',".~~>>!?) | | C. IdentiGcation of components referred to in this LER: |
| Yr??ii!?i@"fg".'I.'s$ | | g>>??( ?0? i',.",R>>S4>>(r0! I? +>>@>>>>? p I??li? ~@"~'>>?)0 Pt~'qg F'P~ 'R??>>'>>>>? ?)?f??I'9? ~ Api',".~~>>!?) Yr??ii!?i @"fg".'I.'s$ j+5'Ligs+rlp'5!'(!)3$)') ?'".0@q'?? |
| j+5'Ligs+rlp'5!'(!)3$ | | ".~R( .~?IREE]805,'8YSTEM<&3'.":~z Electro H draulio Control N/A TG |
| )')?'".0@q'?? | | |
| ".~R(.~?IREE]805,'8YSTEM<&3'.":~z Electro H draulio Control N/A TG t l 4}} | | t l |
| | 4}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML18040A2851993-12-0808 December 1993 LER 93-010-00:on 931108,HPCS Was Inoperable Due to Equipment Deficiency,Inadequate Managerial Methods & Poor Work Practices.Replaced Deficient Contactors & Restored Tap Setting.Also Reportable Per Part 21.W/931208 Ltr ML18038A3191990-08-10010 August 1990 LER 90-006-00:on 891027,discovered Unverified Assumption in App R Safe Shutdown Analysis.Caused by Fire Protection Program Failure to Provide Detailed Procedural Instructions for Operator Actions.New Procedures developed.W/900810 Ltr ML18038A4701989-05-15015 May 1989 LER 89-014-00:on 890413,unit Reactor Experienced Reactor Scram Which Was Result of Turbine Trip Due to Actuation of Generator Protection Circuitry.Turbine Trip Caused by Disconnected Wire.Wire relanded.W/890515 Ltr ML18038A4131988-08-22022 August 1988 LER 88-051-01:on 870813,shutdown Cooling Sys Isolated & Tech Specs 3.4.9.2 Exceeded.Caused by Equipment Failure,Personnel Error & Procedural & Design Deficiencies.Shutdown Cooling Sys Manually restored.W/880822 Ltr ML18038A4051988-07-0101 July 1988 LER 88-024-00:on 880605,ESF Actuation Occurred Due to Resetting of Failed Radiation Monitor Microcomputer.Caused by Lack of Personnel Training.Defective Cards & Modules in RE14B Microcomputer & DRMS Panel replaced.W/880701 Ltr ML18038A3901988-04-12012 April 1988 LER 88-014-00:on 880313,reactor Scram & ESF Actuations Occurred.Caused by Equipment Failure Due to Design Deficiency.Transmitter Replaced W/Upgraded Model & Temporary Mod Performed to Bypass Logic for valves.W/880412 Ltr ML18038A3891988-02-17017 February 1988 LER 88-001-00:on 880120,reactor Scram Occurred Due to Actual Low Water Level Condition.Caused by Design & Personnel Errors.Operator Disciplined & Mod Addressed Inadvertent Feedwater Control Valve lockup.W/880217 Ltr ML18038A7591987-12-22022 December 1987 LER 87-023-00:on 870422,trip of Normal Reactor Bldg Ventilation & Initiation of Emergency Ventilation Occurred. Caused by Personnel Error.Fuse Replaced.On 871123,util Discovered LER Not Submitted for event.W/871222 Ltr ML18038A2581987-06-15015 June 1987 LER 87-025-00:on 870519,secondary Containment Isolation Signal Generated Due to Technician Relanding Lifted Lead Prematurely.Caused by Breakdown in Communications.Gaitronics Phone &/Or Headset Jack installed.W/870615 Ltr ML18004C0061987-04-13013 April 1987 LER 86-002-01:on 861104,procedure N2-OSP-RMC-W0002 Ran for Over 2 H Thereby Violating Tech Specs.Caused by Personnel Error & Procedure Deficiency.Temporary Change Notice Issued to procedure.W/870413 Ltr ML20024E8331983-08-16016 August 1983 LER 83-021/03L-0:on 830720,22,26 & 28,emergency Cooling Sys Loop 11 Taken Out of Svc for Periods Up to 5 H.Caused by Attempt to Reseat Isolation Valve 39-05.Valve Seat Lapped & Loop Returned to svc.W/830819 Ltr ML20024E6341983-08-0202 August 1983 LER 83-017/03L-0:on 830707,HPCI Feedwater Booster Pumps 11 & 13 Taken Out to Svc to Inspect Impellers Due to Similar Problem on nonsafety-related Pump.Parts of Strainer Found in Pumps But Pumps undamaged.W/830805 Ltr ML20024E0251983-07-22022 July 1983 LER 83-019/03L-0:on 830623,two Monthly Surveillance Tests on Inadequate Core cooling-accident Level Monitor Missed Following 811231 Installation.Surveillance Procedures Generated & Added to schedule.W/830725 Ltr ML20024B7711983-06-17017 June 1983 LER 83-010/03L-0:on 830524,core Topping Pump 121 Removed from Svc to Replace Packing.Caused by Air Leaking Due to Iltr Pressure Introduction in Pump.Packing Replaced & Pump Returned to Svc within 22 h.W/830621 Ltr ML19277C5881983-06-16016 June 1983 LER 83-013/03L-0:on 830610,during Routine Surveillance,Lock Found Missing from Outside Inlet Valve 40-12 for Core Spray Sys.Valve & Breaker in Open Position.Lock Missing for No More than 15 Days.Lock replaced.W/830708 Ltr ML20024B7101983-06-16016 June 1983 LER 83-011/03L-0:on 830604,electromatic Relief Valve 121 Failed to Open.Caused by Dirty Pilot Due to Oxide Buildup During Extended Outage.Pilot Cleaned & Retested & Normal Shutdown initiated.W/830628 Ltr ML20023D9571983-05-24024 May 1983 LER 83-009/03L-0:on 830426,control Room Ventilation Sys Removed from Svc for Mods to Control Room Wall,Per LER 83-06.Temporary Flexible Ducting in Place During Mods. Mods Completed.Ventilation Sys Returned to svc.W/830526 Ltr ML20023D2551983-05-11011 May 1983 LER 83-006/03L-0:on 830411,while Performing Design Review, Discovered That Poured Concrete North & West Walls of Control Room Would Not Meet Original Seismic Criteria. Mods Made to Improve Wall Structural Loading Capabilities ML20023B8321983-04-18018 April 1983 LER 81-053/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed ML20028C8391983-01-0505 January 1983 LER 82-018/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20028C8361983-01-0505 January 1983 LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20027C9681982-10-19019 October 1982 LER 82-001 Has Been Canceled ML17341B6651982-08-0505 August 1982 LER 82-011/03L-0:on 820802,oil Leak on Fuel Oil Supply Manifold Discovered on Diesel Fire Pump.Caused by Defective Braze Joint.Leak Repaired by Manufacturer ML20050N6691982-04-0505 April 1982 LER 82-009/01T-0:on 820323,while Conducting Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on Recirculation Piping.Cause Being Investigated ML20050C3881982-03-29029 March 1982 LER 82-008/01T-0:on 820317,review of Surveillance Test N1-ST-R7 Revealed Potential for Reactor Steam to Leak to Atmosphere from Emergency Condenser Vents.Caused by Potential Sys Leaks.Sys Modified Per NUREG-0737 Item II.B.1 ML20052F8991982-03-24024 March 1982 LER 82-009:on 820323,during Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on 11 Recirculation Piping Suction from Reactor Vessel.Cause Under Investigation ML20042C5041982-03-23023 March 1982 LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate ML20052F8461982-03-18018 March 1982 LER 82-008:on 820317,discovered Potential Path for Reactor Steam from Emergency Condenser Steam Line Vents to Atmosphere If Emergency Condenser Tube Leaks Occur.Caused by Mods Made to Comply w/NUREG-0737,Item II.B.1 ML20042A6891982-03-12012 March 1982 LER 82-007/04L-0:on 820222,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity Was Determined Not Met for Nov 1981.Cause Not Stated.Tech Spec Proposal Being Submitted to Update Stds ML20049H6101982-02-19019 February 1982 LER 82-005/03L-0:on 820208,115 Kv Line Taken Out of Svc for Maint,Placing Plant in Limited Condition of Operation.Maint on Line Required Due to Open Loop.Line Repaired & Returned to Svc ML20041C1651982-02-19019 February 1982 LER 82-004/01T-0:on 820207,during Routine 115-KV Breaker Exercising,Ground Directional Relay Caused Opening of Breaker Alternate 115-KV.Caused by Momentary Loss Offsite Power.Power Restored After Closing Oswego-NMP1 Breaker ML20041C1171982-02-17017 February 1982 LER 82-003/01T-0:on 820204,at 100% Power,Reactor Bldg Ventilation Sys Isolated & Emergency Ventilation Sys Initiated Due to Radioactive Release.Caused by Overflow of Reactor Water Cleanup Sys Filter Sludge Tank ML20041A7511982-02-10010 February 1982 LER 82-002/01T-0:on 820129,NRC Inspector Discovered That Primary Containment Following DBA LOCA May Not Be Vented Using Operating Procedure Due to Inaccessibility of Reactor Bldg.Combustible Gas Control Sys Will Be Installed ML20052F8961982-02-0808 February 1982 LER 82-004:on 820207,during Steady State Operation,Momentary Loss of 115 Kv Offsite Power Caused Emergency Diesel Generators to auto-start on Low Voltage to Power Boards 102 & 103 ML20052F8981982-02-0505 February 1982 LER 82-003:on 820204,during Steady State Operation,Cleanup Sludge Tank Vent Overflowed Into Reactor Bldg Exhaust Ventilation Sys Causing Emergency Ventilation Sys to Initiate.Cause Not Stated.Decontamination in Progress ML20052F8931982-02-0101 February 1982 LER 82-002:on 820129,during Steady State Power,Upon Review by Resident Inspector,Discovered That Operating Procedure Describing Steps to Vent Primary Containment Following DBA LOCA Required Personnel to Enter Reactor Bldg ML20040B8621982-01-18018 January 1982 LER 81-054/03L-0:on 811221,insertion of Shallow Control Rods Resulted in Average Planar Linear Heat Generation Rate in Excess of Tech Spec Limits.Caused by Flux Coupling Between Control Rods.Extra Rods Inserted & Tech Specs Modified ML20039E2951982-01-0202 January 1982 LER 81-025,is Cancelled ML20039C0951981-12-14014 December 1981 LER 81-053/03L-0:on 811120,emergency Condensers 11 & 12 Were Isolated When Emergency Condenser Vent Radiation Monitor de-energized Due to Loss of Dc Motor Speed Control.Caused by Defective Silicon Controlled Rectifier.Rectifier Replaced ML20038B4971981-11-25025 November 1981 LER 81-008/01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable ML20038B4561981-11-25025 November 1981 LER 81-050/03L-0:on 810715,reactor Bldg Ventilation Duct Radiation Monitor Showed Abnormal Spiking Which Initiated Emergency Ventilation Sys.Caused by Malfunctioning sensor-convertor Unit.Unit Replaced & Calibr ML20038B8801981-11-24024 November 1981 LER 81-052/03L-0:on 810812,failure of One Reactor Vessel Electromatic Relief Valve Thermocouple & Two Reactor Vessel Head Safety Valve Thermocouples Noted in Testing.Cause to Be Investigated Given Drywell Access in Next Cold Shutdown ML20038B7701981-11-24024 November 1981 LER 81-049/03L-0:on 811112,during Normal Operation,Feedwater Hydraulic Snubber 29-HS-6 Taken Out of Svc for Preventative Maint Because of Small Oil Leak.Cause Not Stated.Snubber Rebuilt & Returned to Svc ML20038B4581981-11-20020 November 1981 LER 81-051/04L-0:on 811109,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity (LLD) Not Met.Caused by Higher LLD Values When Test Data Converted from Wet to Dry Weight Units ML20011A4851981-09-30030 September 1981 LER 81-046/04T-0:on 810922,review of 810813 & 14 ETS Semiannual Samples of Cladophora Showed Co-60 & Nb-95 at Level of 10 Times Control Value.Probably Caused by Liquid Effluent Discharge & Oct 1980 Chinese Weapons Test ML20010G6931981-09-10010 September 1981 LER 81-042/04T-0:on 810831,during Weekly Environ Radiation Monitor Insp,Only Six Monitors Found Functioning Due to Defective Power Supply Units.Cause Unknown.Portable Monitor Installed ML20010G4341981-09-0404 September 1981 LER 81-040/03L-0:on 810818,chromated Water Found in Diesel Generator 102 Raw Water Due to Water Leaking Through Heat Exchangers.Cause Unknown.Raw Water Lines Drained & All Chromate Recovered 1998-07-02
[Table view] Category:RO)
MONTHYEARML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML18040A2851993-12-0808 December 1993 LER 93-010-00:on 931108,HPCS Was Inoperable Due to Equipment Deficiency,Inadequate Managerial Methods & Poor Work Practices.Replaced Deficient Contactors & Restored Tap Setting.Also Reportable Per Part 21.W/931208 Ltr ML18038A3191990-08-10010 August 1990 LER 90-006-00:on 891027,discovered Unverified Assumption in App R Safe Shutdown Analysis.Caused by Fire Protection Program Failure to Provide Detailed Procedural Instructions for Operator Actions.New Procedures developed.W/900810 Ltr ML18038A4701989-05-15015 May 1989 LER 89-014-00:on 890413,unit Reactor Experienced Reactor Scram Which Was Result of Turbine Trip Due to Actuation of Generator Protection Circuitry.Turbine Trip Caused by Disconnected Wire.Wire relanded.W/890515 Ltr ML18038A4131988-08-22022 August 1988 LER 88-051-01:on 870813,shutdown Cooling Sys Isolated & Tech Specs 3.4.9.2 Exceeded.Caused by Equipment Failure,Personnel Error & Procedural & Design Deficiencies.Shutdown Cooling Sys Manually restored.W/880822 Ltr ML18038A4051988-07-0101 July 1988 LER 88-024-00:on 880605,ESF Actuation Occurred Due to Resetting of Failed Radiation Monitor Microcomputer.Caused by Lack of Personnel Training.Defective Cards & Modules in RE14B Microcomputer & DRMS Panel replaced.W/880701 Ltr ML18038A3901988-04-12012 April 1988 LER 88-014-00:on 880313,reactor Scram & ESF Actuations Occurred.Caused by Equipment Failure Due to Design Deficiency.Transmitter Replaced W/Upgraded Model & Temporary Mod Performed to Bypass Logic for valves.W/880412 Ltr ML18038A3891988-02-17017 February 1988 LER 88-001-00:on 880120,reactor Scram Occurred Due to Actual Low Water Level Condition.Caused by Design & Personnel Errors.Operator Disciplined & Mod Addressed Inadvertent Feedwater Control Valve lockup.W/880217 Ltr ML18038A7591987-12-22022 December 1987 LER 87-023-00:on 870422,trip of Normal Reactor Bldg Ventilation & Initiation of Emergency Ventilation Occurred. Caused by Personnel Error.Fuse Replaced.On 871123,util Discovered LER Not Submitted for event.W/871222 Ltr ML18038A2581987-06-15015 June 1987 LER 87-025-00:on 870519,secondary Containment Isolation Signal Generated Due to Technician Relanding Lifted Lead Prematurely.Caused by Breakdown in Communications.Gaitronics Phone &/Or Headset Jack installed.W/870615 Ltr ML18004C0061987-04-13013 April 1987 LER 86-002-01:on 861104,procedure N2-OSP-RMC-W0002 Ran for Over 2 H Thereby Violating Tech Specs.Caused by Personnel Error & Procedure Deficiency.Temporary Change Notice Issued to procedure.W/870413 Ltr ML20024E8331983-08-16016 August 1983 LER 83-021/03L-0:on 830720,22,26 & 28,emergency Cooling Sys Loop 11 Taken Out of Svc for Periods Up to 5 H.Caused by Attempt to Reseat Isolation Valve 39-05.Valve Seat Lapped & Loop Returned to svc.W/830819 Ltr ML20024E6341983-08-0202 August 1983 LER 83-017/03L-0:on 830707,HPCI Feedwater Booster Pumps 11 & 13 Taken Out to Svc to Inspect Impellers Due to Similar Problem on nonsafety-related Pump.Parts of Strainer Found in Pumps But Pumps undamaged.W/830805 Ltr ML20024E0251983-07-22022 July 1983 LER 83-019/03L-0:on 830623,two Monthly Surveillance Tests on Inadequate Core cooling-accident Level Monitor Missed Following 811231 Installation.Surveillance Procedures Generated & Added to schedule.W/830725 Ltr ML20024B7711983-06-17017 June 1983 LER 83-010/03L-0:on 830524,core Topping Pump 121 Removed from Svc to Replace Packing.Caused by Air Leaking Due to Iltr Pressure Introduction in Pump.Packing Replaced & Pump Returned to Svc within 22 h.W/830621 Ltr ML19277C5881983-06-16016 June 1983 LER 83-013/03L-0:on 830610,during Routine Surveillance,Lock Found Missing from Outside Inlet Valve 40-12 for Core Spray Sys.Valve & Breaker in Open Position.Lock Missing for No More than 15 Days.Lock replaced.W/830708 Ltr ML20024B7101983-06-16016 June 1983 LER 83-011/03L-0:on 830604,electromatic Relief Valve 121 Failed to Open.Caused by Dirty Pilot Due to Oxide Buildup During Extended Outage.Pilot Cleaned & Retested & Normal Shutdown initiated.W/830628 Ltr ML20023D9571983-05-24024 May 1983 LER 83-009/03L-0:on 830426,control Room Ventilation Sys Removed from Svc for Mods to Control Room Wall,Per LER 83-06.Temporary Flexible Ducting in Place During Mods. Mods Completed.Ventilation Sys Returned to svc.W/830526 Ltr ML20023D2551983-05-11011 May 1983 LER 83-006/03L-0:on 830411,while Performing Design Review, Discovered That Poured Concrete North & West Walls of Control Room Would Not Meet Original Seismic Criteria. Mods Made to Improve Wall Structural Loading Capabilities ML20023B8321983-04-18018 April 1983 LER 81-053/03L-1:on 811120,discovered That Single Failure of Electrical Power Supply Could Either Isolate Both Condenser Sys or Cause Failure to Isolate.Logic for Initiation & Isolation of Condenser Sys Reviewed ML20028C8391983-01-0505 January 1983 LER 82-018/03L-0:on 821207,during Maint Outage,Leakage from Valves 68-05 & 68-08 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20028C8361983-01-0505 January 1983 LER 82-017/03L-0:on 821206,during Maint Outage,Leakage from Valves 68-06 & 68-09 Found Exceeding Tech Specs.Caused by Poor Seal Design.Mods Will Be Completed During Current Outage & Followed by Retest ML20027C9681982-10-19019 October 1982 LER 82-001 Has Been Canceled ML17341B6651982-08-0505 August 1982 LER 82-011/03L-0:on 820802,oil Leak on Fuel Oil Supply Manifold Discovered on Diesel Fire Pump.Caused by Defective Braze Joint.Leak Repaired by Manufacturer ML20050N6691982-04-0505 April 1982 LER 82-009/01T-0:on 820323,while Conducting Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on Recirculation Piping.Cause Being Investigated ML20050C3881982-03-29029 March 1982 LER 82-008/01T-0:on 820317,review of Surveillance Test N1-ST-R7 Revealed Potential for Reactor Steam to Leak to Atmosphere from Emergency Condenser Vents.Caused by Potential Sys Leaks.Sys Modified Per NUREG-0737 Item II.B.1 ML20052F8991982-03-24024 March 1982 LER 82-009:on 820323,during Routine Reactor Vessel Hydrostatic Testing Prior to Startup,Water Observed Leaking from Insulation on 11 Recirculation Piping Suction from Reactor Vessel.Cause Under Investigation ML20042C5041982-03-23023 March 1982 LER 82-006/04L-0:on 820225,during Normal Operation,While Tempering Plant Inlet Canal,Plant Discharge Temp Exceeded 85 F.Caused by Increase in Lake Temp Due to Weather Conditions & Inability to Fully Lower Tempering Gate ML20052F8461982-03-18018 March 1982 LER 82-008:on 820317,discovered Potential Path for Reactor Steam from Emergency Condenser Steam Line Vents to Atmosphere If Emergency Condenser Tube Leaks Occur.Caused by Mods Made to Comply w/NUREG-0737,Item II.B.1 ML20042A6891982-03-12012 March 1982 LER 82-007/04L-0:on 820222,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity Was Determined Not Met for Nov 1981.Cause Not Stated.Tech Spec Proposal Being Submitted to Update Stds ML20049H6101982-02-19019 February 1982 LER 82-005/03L-0:on 820208,115 Kv Line Taken Out of Svc for Maint,Placing Plant in Limited Condition of Operation.Maint on Line Required Due to Open Loop.Line Repaired & Returned to Svc ML20041C1651982-02-19019 February 1982 LER 82-004/01T-0:on 820207,during Routine 115-KV Breaker Exercising,Ground Directional Relay Caused Opening of Breaker Alternate 115-KV.Caused by Momentary Loss Offsite Power.Power Restored After Closing Oswego-NMP1 Breaker ML20041C1171982-02-17017 February 1982 LER 82-003/01T-0:on 820204,at 100% Power,Reactor Bldg Ventilation Sys Isolated & Emergency Ventilation Sys Initiated Due to Radioactive Release.Caused by Overflow of Reactor Water Cleanup Sys Filter Sludge Tank ML20041A7511982-02-10010 February 1982 LER 82-002/01T-0:on 820129,NRC Inspector Discovered That Primary Containment Following DBA LOCA May Not Be Vented Using Operating Procedure Due to Inaccessibility of Reactor Bldg.Combustible Gas Control Sys Will Be Installed ML20052F8961982-02-0808 February 1982 LER 82-004:on 820207,during Steady State Operation,Momentary Loss of 115 Kv Offsite Power Caused Emergency Diesel Generators to auto-start on Low Voltage to Power Boards 102 & 103 ML20052F8981982-02-0505 February 1982 LER 82-003:on 820204,during Steady State Operation,Cleanup Sludge Tank Vent Overflowed Into Reactor Bldg Exhaust Ventilation Sys Causing Emergency Ventilation Sys to Initiate.Cause Not Stated.Decontamination in Progress ML20052F8931982-02-0101 February 1982 LER 82-002:on 820129,during Steady State Power,Upon Review by Resident Inspector,Discovered That Operating Procedure Describing Steps to Vent Primary Containment Following DBA LOCA Required Personnel to Enter Reactor Bldg ML20040B8621982-01-18018 January 1982 LER 81-054/03L-0:on 811221,insertion of Shallow Control Rods Resulted in Average Planar Linear Heat Generation Rate in Excess of Tech Spec Limits.Caused by Flux Coupling Between Control Rods.Extra Rods Inserted & Tech Specs Modified ML20039E2951982-01-0202 January 1982 LER 81-025,is Cancelled ML20039C0951981-12-14014 December 1981 LER 81-053/03L-0:on 811120,emergency Condensers 11 & 12 Were Isolated When Emergency Condenser Vent Radiation Monitor de-energized Due to Loss of Dc Motor Speed Control.Caused by Defective Silicon Controlled Rectifier.Rectifier Replaced ML20038B4971981-11-25025 November 1981 LER 81-008/01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable ML20038B4561981-11-25025 November 1981 LER 81-050/03L-0:on 810715,reactor Bldg Ventilation Duct Radiation Monitor Showed Abnormal Spiking Which Initiated Emergency Ventilation Sys.Caused by Malfunctioning sensor-convertor Unit.Unit Replaced & Calibr ML20038B8801981-11-24024 November 1981 LER 81-052/03L-0:on 810812,failure of One Reactor Vessel Electromatic Relief Valve Thermocouple & Two Reactor Vessel Head Safety Valve Thermocouples Noted in Testing.Cause to Be Investigated Given Drywell Access in Next Cold Shutdown ML20038B7701981-11-24024 November 1981 LER 81-049/03L-0:on 811112,during Normal Operation,Feedwater Hydraulic Snubber 29-HS-6 Taken Out of Svc for Preventative Maint Because of Small Oil Leak.Cause Not Stated.Snubber Rebuilt & Returned to Svc ML20038B4581981-11-20020 November 1981 LER 81-051/04L-0:on 811109,while Reviewing Environ Radiation Fish Analysis Sample Data,Lower Limit of Detection Sensitivity (LLD) Not Met.Caused by Higher LLD Values When Test Data Converted from Wet to Dry Weight Units ML20011A4851981-09-30030 September 1981 LER 81-046/04T-0:on 810922,review of 810813 & 14 ETS Semiannual Samples of Cladophora Showed Co-60 & Nb-95 at Level of 10 Times Control Value.Probably Caused by Liquid Effluent Discharge & Oct 1980 Chinese Weapons Test ML20010G6931981-09-10010 September 1981 LER 81-042/04T-0:on 810831,during Weekly Environ Radiation Monitor Insp,Only Six Monitors Found Functioning Due to Defective Power Supply Units.Cause Unknown.Portable Monitor Installed ML20010G4341981-09-0404 September 1981 LER 81-040/03L-0:on 810818,chromated Water Found in Diesel Generator 102 Raw Water Due to Water Leaking Through Heat Exchangers.Cause Unknown.Raw Water Lines Drained & All Chromate Recovered 1998-07-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059B9051998-02-28028 February 1998 NMP Unit 1 Boat Samples Analyses Part Iii:Tension Tests, RDD:98:55863-004-000:01 1999-09-30
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NIAGARA MOHAWK G EN ERATION NINE MILE POINT NUCLEAR STATION/lAKEROAD, P.O. BOX 63, LYCOMING, NEW YORK 13093 BUSINESS GROUP dune 4, 1998
'NNP2L 1788 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE: Docket No. 50-410 LER 98-04, Supplement 1 Gentlemen:
In accordance with 10CFR50.73 (a)(2)(i)(B), we are submitting LER 98-04, Supplement 1, "Missed Technical Specification Required LSFT of Level 8 Trip of Main Turbine." This supplement is to clarify actions taken to correct the cause of knowledge deficiency.
Very truly yours, Kim A. Dahlberg, Plant Manager - NhG?2 KAD/GJG/kap Attachment xc: Mr. H. J. Miller, Regional Administrator, Region I Mr. B. S. Norris, Senior Resident Inspector Records Management 9806ihoi40 0 50004ie PDR ADQCK S
0 REGULATORY COMMISSION ROVED OMB NO; 3!500lcl EXPIRES:
ESfJMATKD BURDEN PER RESPONSE TO COMPLY Wml TlBS INFORMATIONCOLLECIION LICENSEE EVENT REPORT (LER) REQUESf c 50AJ HRS. FORWARD COMMENIS REGARDOIO BURDEN ESAMATKTO TIES RECORDS AND REPORTS MANAGEMENfBRANCJ I (M30), U.S. NUCLEAR REGULATORY COMMlSS ION, WAS) BNGION, DC 3M55, ANDTO THE PAPERWORK REDUCIION PROJECT O1500104), OFF)CHOP MANAGEMENfAND BUDGBI; WASHINGION, DC 30503 FACK1IYNAME (I) DOCXEf NUMBER (D PAGE O)
Nine Mile Point Unit 2 05000410 1 OF 4 TIILE (4)
Missed Technical Specification Required LSFT of Level 8 Trip of Main Turbine EVENI'ATE(5) REPORT DATEG) OTHER FACILmES INVLVED(I)
MONIH DAY* YEAR gag REVISION MONBl DAY YEAR FACJLIIYNAMES NUMBER 03 02 98 98 0 1 06 04 98 N/A 05000 N/A 05000 OPERATING MODB (9) TIES REPORT IS SUBMIITIXIPURSUANT TO THK REQUIREMENIS OF IO CFR 5: (CJ>cca c>>c c>cc>>c>cc c/dscfcJJ>>wJ>>I) (II)
POWER LEVEL (lc) 0 20.2201(b) 0 20.2203(a)(2)(v) 3 50.73(a)(2)Q 0 50.73(a)(2)(viii) 0 20.2203(a)(1) 0 20.2203(a)(3) Q 0 50.73(a)(2)(ii) 0 50.73(a)(2)(x) 0 20.2203(a)(2)Q 0 20.2203(a)(3)(ii) 0 $ 0.73(a)(2)(iii) 073.7i 0 20.2203(a)(2)(ii) 0 20.2203(a)(4) 0 $ 0.73(a)(2)(v) 0 orHHt 0 20.2203(a)(2)(iii) 0 50.36(c)(1) 0 50.73(a)(2)(v) J>CccU> I>c >Ilcc>occ aclo>>> ccc>J Fcc>>c 555U J>c roc, J>BC J>YK~>~W 0 20.2203(a)(2)(iv) 0 50.36(c)(2) 0 50.73(a)(2)(vii)
LICENSEE CONfACf FORTIES LKR (l1) .
NAME TKIZPHONB NUMBER K. D. Ward - Technical Support Manager (315) 349-1043 COMPLEIKONB ISNB FOR EACH COMPONENf FAILURE DESCRIBED IN TIES REPORT (I3)
REPORTABLB TO NPRDS SUPPLKMKNFALREPORT EXPECIKD 0O EXPIATED MONIH DAY SUBMISSION DATE (l5) 0 YES Q'ycc, co>tpkcc ZXFECIKDS Jtul5SJOJVJMIF>J 5 ABSTRACT ghsltco140cPc>ccc>ac> FFccc(>>~JJcj(/Jcasc0>IJccN>cc~ JJ>>cc) 06)
On March 2, 1998, Niagara Mohawk Power Corporation (NMPC) determined that the Nine Mile Point Unit 2 (MMP2) Logic System Functional Tests (LSFT) for the main turbine trip on high reactor vessel level (Level 8) failed to verify the entire circuit. This is a violation of Technical Specification Surveillance Requirement (TS SR) 4.3.9.2 which is required to be performed at least once per 18 months.
The cause of this event has been determined to be an apparent knowledge deficiency of the Electro Hydraulic Control (EHC) system combined with poor work practices, which led the LSFT procedure developers to conclude that the EHC panel was the actuated device. Contributing to this event was the omission of relevant information when the LSFT procedure for the Level 8 turbine trip was developed. The circuit diagrams for the Level 8 turbine trip show the EHC panel as a circuit termination.
The applicable LSFT procedures will be revised prior to refueling outage 6 (RFO6). This event has been discussed with personnel performing the Generic Letter 96-01 procedure reviews.
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FACILIIYNAME(I) PAGE O)
YEAR REVISION
$ NUMBER Nine Mile Point Unit 2 05000410 98 04 0 1 02 OF 04 TE)ff Qnsarv tPtttt lt ttyket, sr@ ofdMasd NRC iona SSSI's) P D On March 2, 1998, Niagara Mohawk Power Corporation (NMPC) determined that the Nine Mile Point Unit 2 (NMP2) Logic System Functional Tests (LSFT) for the main turbine trip on high reactor vessel level (Level 8) failed to verify the entire circuit. This is a violation of Technical Specification Surveillance Requirement (TS SR) 4.3.9.2 which is required to be performed at least once per 18 months.
This deficiency was identified in response to a question from another licensee concerning LSFT testing of the Electro Hydraulic Control (EHC) system. The EHC system engineer reviewed the LSFT drawings and determined that the EHC circuit had been tested from the Level 8 transmitter to an EHC panel in accordance with an LSFT procedure which references TS 4.3.9.2. The circuitry from the master trip bus within the EHC panel to the turbine stop and control valves was tested in accordance with an Instrument and Control surveillance procedure which did not specifically reference TS 4.3.9.2. However, the circuitry from the EHC panel input terminals to the master trip bus was not tested in either of the LSFT procedures.
After further review, it was found that the EHC panel circuitry from the input terminals to the master trip bus has been tested since Refueling Outage 3 in October 1993, but not by an LSFT. Work orders have been initiated with step text to perform the testing each refueling outage since RFO3. Therefore, the entire circuit has been tested since October 1993 to meet the LSFT requirements.
NMPC had performed two previous LSFT reviews and an initial review of this Level 8 LSFT as part of the overall LSFT review for Generic Letter (GL) 96-01. None of these reviews identified this deficiency.
However, the NhP2 GL 96-01 process has not been completed. A senior engineer is required to perform an independent verification of the initial reviewer's work. That verification would likely have identified this deficiency.
The cause of this event has been determined to be an apparent knowledge deficiency of the EHC system combined with poor work practices, which led the LSFT procedure developers to conclude that the EHC panel was the actuated device. Contributing to this event,was the omission of relevant information when the LSFT procedure for the Level 8 turbine trip was developed. The circuit diagrams for the Level 8 turbine trip show the EHC panel as a circuit termination.
The cause of the individual not finding this during the initial GL 96-01 review was again knowledge deficiency and poor work practice. The individual believed that since the EHC/Turbine System is non-safety related, the actual trip of the main turbine was simply an economic issue to prevent turbine damage and not for reactor safety. Based on this, the individual did not pursue his review beyond the EHC panel input.
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ESTIMATED BURDEN PER RESPONSB TO COMPLY WIBITlBS INFORMATIONCOLLKCIION LICENSEE EVENT REPORT (LER) RE(IUESF: SOA) HRS. FORWARD COMMENTS REGARDB(G BURDEN ESIIMATETOTHE TEXT CONTINUATION RECORDS AND REPORTS MANAGEMKNI'RANCH(P>>030), UA. REGULATORY COMMISSION, WASIBNQION>> DC 30SSS, ANDTO TIIE PAPERWORK REDUCIION PROJKCP (IIS00104)>> OFFICE OP MANAGEMENIAND BUDGET>> WASIBNGION>> DC 30S03.
FACLIIYNAME (I) LKR NUMBER (6) PAGE(3)
SEQUENIIAL REVISION NUMBER NUMBER Nine Mile Point Unit 2 05000410 98 04 0 1 03 OF 04 TEXT Q'~ apace 4 reqafraf, me ok5danaf NRC F~ 30' 's) (II)
This event is reportable in accordance with 10CFR50.73(a)(2)(i)(B), "any operation or condition prohibited by the plant's Technical Specifications."
The purpose of the turbine trip on high water level is to cause a reactor scram to limit the minimum critical power ratio. NMP2 Updated Safety Analysis Report (USAR) Section 15.1.2, Feedwater Controller Failure-Maximum Demand, Subsection 15.1.2.2.3, Effect of Single Failures and Operator Errors, states "In Table 15.1-3, the first sensed event to initiate corrective action to the transient is the vessel high water level (L8) trip. Multiple level sensors are used to sense and detect when the water level reaches the L8 setpoint. At this point in the logic, a single failure will not initiate or prevent a turbine trip signal. Turbine trip signal transmission, however, is not built to single-failure criterion. The result of a failure at this point would have the effect of delaying the pressurization "signature." However, high moisture levels entering the turbine will be detected by high levels in the turbine s moisture separators, resulting in a trip of the unit." In addition, excessive moisture entering the turbine will cause vibration to the point where it too will trip the unit."
Based upon these other turbine trip signals and associated reactor scram, the impact of not having this Level 8 trip is negligible. Therefore, this event did not pose a threat to public health and safety or to plant personnel.
The applicable LSFT procedures willbe revised prior to next use.
- 2. This event has been reviewed and expectations reinforced with the personnel performing the GL 96-01 procedure reviews. The purpose of this review was to assure that personnel clearly understand that an LSFT is required to test from initiating device to the actuated device.
The verification process for GL 96-01 willspecifically address the LSFT circuit scope as part of the verification review. The verification reviews are scheduled for completion by the end of RFO6.
Since the personnel who originally developed the EHC-LSFT procedures are no longer employed at NMPC, and Corrective Action 2 assured a thorough review, no additional training is warranted.
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SEQUENfIAL REVISION NUMBER NUMBER Nine Mile Point Unit 2 05000410 98 04 0 1 04 OF 04 TExT Q'score 4F>>>>c!4 v te>>p(>>ef, are okbfaad hRc Fme 3!Is('sJ p D V.
A. Failed components: none.
B. Previous similar events:
NMP2 has had a number of instances where procedure preparation or review caused missed or inadequately performed surveillance tests. In accordance with NMPC's Corrective Action Program, a Deviation/Event Report (DER) was initiated to evaluate this trend. A root cause team was assembled to evaluate this overall trend to determine ifprocess problems or other common aspects could be identified. Required corrective actions willbe taken as necessary to correct any identified deficiencies in accordance with the corrective action program.
C. IdentiGcation of components referred to in this LER:
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