PNO-II-97-065, on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG

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PNO-II-97-065:on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG
ML20197F622
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 12/29/1997
From: Lesser M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
References
PNO-II-97-065, PNO-II-97-65, NUDOCS 9712300258
Download: ML20197F622 (1)


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December 29, 1997 ZRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PHO-II-97-065 Thic preliminary notification constitutes EARLY notice of events of POSSIBLE i cefoty or public interest significance. The information is as initially rocoived without verification or evaluation, and is basically all that is '

known by Region II staff in Atlanta, Georgia on this date.

EA!1111tv Liggr ,es_Emeraency Classification '

Duko Power Co. Nt fication of Unusual Event Oconee 1 A1..t Sonoca, South Carolina Site Area Emergency Dockets: 50-269 General Emergency X Not Applicable Subjects STEAM GENERATOR (SG) 1A TUBE LEAK >

On December 28, 1997, Oconee Unit I was escalating in power while returning from a refueling nutage. The unit was at about 54% power when it was determined that the 1A steam generator had a potential tube leak baned upon an increasing trend on ,-team line and steam jet air ejector

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radiation monitors. A sample indicated a leakage o.' about 400 gallons per day (gpd).

At i The licensee entered their SG tube leak procedure at 3:00 p.m.

3:07 p.m., upon confirming the 400 gpd leak rate, the licensee initiated a controlled shutdown of the unit due to exceeding the technical specification leakage limit of 150 gpd. The reactor was shut down at 4:? p.m. The licensee is continuing with plant depressurization and covidown and is in the process of planning an outage of several days to investigate and repair the steam generator. A small release of radioactivity to the atmosphere was monitored and is estimated to total 1.97 E-2 Curies, well below permissible levels.

The State of' South Carolina was notified by the NRC. i The NRC received initial notification of this event by telephone from the licensee at 3:32 p.m. (EST) on December 28, 1997.

Th:is information is current as of 10:30 a.m. (EST) on December 29, 1997.

The resident inspectors responded to the site and confirmed licensee actions.

Cor.t a ct : M. LESSER i (404)562-4560 ,

9712300258 971229 "

PDR IbE PNO-II-97-065 PDR_ ,

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