Notice of Violation from Insp on 910312-15.Violations Noted:Station Was Not Maintained According to Main Procedure MP/0/A/1800/105,Section 6.5,which Clearly Identified That Flange Was to Be Installed on Valve 3LP19ML20134D258 |
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Oconee ![Duke Energy icon.png](/w/images/7/75/Duke_Energy_icon.png) |
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06/04/1991 |
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NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
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ML20134D255 |
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50-269-91-08, 50-269-91-8, 50-270-91-08, 50-270-91-8, 50-287-91-08, 50-287-91-8, EA-91-049, EA-91-49, NUDOCS 9610210053 |
Download: ML20134D258 (2) |
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Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20211K9431997-09-26026 September 1997 Notice of Violation from Insp on 970721-26.Violation Noted: Licensee Failed to Follow Procedures for Security Badges & Access Control of Facility ML20210S0391997-08-27027 August 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $330,000.Violation Noted:Between 970501-02,w/ Fuel in Oconee Unit 3 Core & RCS Temp Greater than 350 F, Licensee Failed to Maintain HPI Sys Operable as Required ML20134D2581991-06-0404 June 1991 Notice of Violation from Insp on 910312-15.Violations Noted:Station Was Not Maintained According to Main Procedure MP/0/A/1800/105,Section 6.5,which Clearly Identified That Flange Was to Be Installed on Valve 3LP19 ML20207T5431987-03-12012 March 1987 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000.Noncompliance Noted:Measures Not Established to Assure That Regulatory Requirements & Design Bases Correctly Translated Into Specs,Drawings & Procedures ML20211A4991987-02-11011 February 1987 Notice of Violation from Insps on 870112-16 ML20210U3211987-02-0505 February 1987 Notice of Violation from Insp on 861015-1110.Violation Noted:For Periods in 1978,1981 & 1986 When Lake Keowee Elevation Less than 792 Ft,Emergency Condenser Cooling Water Sys Inoperable & Unable to Provide Sustained Siphon Flow ML20211A0871987-02-0303 February 1987 Notice of Violation from Insp on 870105-08 ML20212F5511986-12-24024 December 1986 Notice of Violation from Insp on 861103-12 ML20199H4661986-03-27027 March 1986 Notice of Violation from Insp on 860224-28 ML20210H3741986-03-21021 March 1986 Notice of Violation from Insp on 860114-0210 ML20214D7201986-02-19019 February 1986 Notice of Violation from Insp on 851216-20 ML20137U5261986-02-12012 February 1986 Notice of Violation from Insp on 851210-860113 ML20137E3821985-11-22022 November 1985 Notice of Violation from Insp on 851008-1111 ML20133C7351985-10-0101 October 1985 Notice of Violation from Insp on 850903-06 IR 05000813/20090091985-09-16016 September 1985 Notice of Violation from Insp on 850813-0909 ML20132C1851985-09-13013 September 1985 Notice of Violation from Insp on 850729-0802 ML20135D5841985-08-28028 August 1985 Notice of Violation from Insp on 850709-0812 ML20125B5471985-06-0606 June 1985 Notice of Violation from Insp on 850211-0310 IR 05000411/20050131985-06-0303 June 1985 Notice of Violation from Insp on 850411-0513 ML20127N7301985-05-20020 May 1985 Notice of Violation from Insp on 850422-26 ML20127F1021985-04-0909 April 1985 Notice of Violation from Insp on 850318-21 ML20132B0651985-01-23023 January 1985 Notice of Violation from Insp on 841126-30 ML20129H3211984-11-23023 November 1984 Notice of Violation from Insp on 840910-14 ML20058H5731982-06-16016 June 1982 Notice of Violation from Insp on 820510-14 ML20054K3371982-05-0303 May 1982 Notice of Violation from Insp on 820310-0410 1997-09-26
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-II-97-065, on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG1997-12-29029 December 1997 PNO-II-97-065:on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG ML20211K9431997-09-26026 September 1997 Notice of Violation from Insp on 970721-26.Violation Noted: Licensee Failed to Follow Procedures for Security Badges & Access Control of Facility ML20210S0391997-08-27027 August 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $330,000.Violation Noted:Between 970501-02,w/ Fuel in Oconee Unit 3 Core & RCS Temp Greater than 350 F, Licensee Failed to Maintain HPI Sys Operable as Required PNO-II-97-034, on 970613,extended Shutdown to Meet CAL 2-97-03 Commitments to Shutdown Unit 1 No Later than 970614 & to Implement Actions Re HPI Sys.Nrc Resident Inspector Will Followup on Unit 1 Shutdown & Recovery Activities1997-06-13013 June 1997 PNO-II-97-034:on 970613,extended Shutdown to Meet CAL 2-97-03 Commitments to Shutdown Unit 1 No Later than 970614 & to Implement Actions Re HPI Sys.Nrc Resident Inspector Will Followup on Unit 1 Shutdown & Recovery Activities IR 05000269/19930321994-01-0606 January 1994 Insp Repts 50-269/93-32,50-270/93-32,50-287/93-32, 50-369/93-31,50-370/93-31,50-413/93-35 & 50-414,respectively on 931213-17.Violations Noted.Major Areas Inpected:Licensee Safeguards Info Program to folow-up on Licensee Repts PNO-II-93-039, on 930823,reactor Trip Occurred Due to Loss of Power to Vital Panelboard.Investigation Team Dispatched to Site to Review Root Cause & Plant Response.State & Local Authorities Notified1993-08-24024 August 1993 PNO-II-93-039:on 930823,reactor Trip Occurred Due to Loss of Power to Vital Panelboard.Investigation Team Dispatched to Site to Review Root Cause & Plant Response.State & Local Authorities Notified IR 05000269/19930061993-03-22022 March 1993 Partially Withheld Insp Repts 50-269/93-06,50-270/93-06 & 50-287/93-06 on 930222-25 (Ref 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Licensee Physical Security Program for Power Reactors IR 05000269/19930011993-02-0101 February 1993 Safeguards Insp Repts 50-269/93-01,50-270/93-01 & 50-287/93-01 on 930104-07.No Violations Noted.Major Areas Inspected:Physical Security Program.Details Withheld (Ref 10CFR73.21) IR 05000269/19920251992-12-0303 December 1992 Insp Repts 50-269/92-25,50-270/92-25 & 50-287/92-25 on 921102-06.No Violations or Deviations Noted.Major Areas Inspected:Physical Security Program for Power Reactors, Audits,Protected & Vital Area Barriers.Details Withheld PNO-II-92-070, on 921019,several Circuit Breakers Failed in 230KV Switchyard to Open Position for Unknown Reasons. Licensee Has Inititated Investigation to Review Event to Determine Cause & Determine Why Certain Equipment Failed1992-10-20020 October 1992 PNO-II-92-070:on 921019,several Circuit Breakers Failed in 230KV Switchyard to Open Position for Unknown Reasons. Licensee Has Inititated Investigation to Review Event to Determine Cause & Determine Why Certain Equipment Failed PNO-II-91-074B, on 911123,unit Remained in Cold Shutdown,Per Declaration of Alert at 0214 Due to Leak in Rcs.As of 911126,total of 7,800 Gallons of Treated Water Released from Plant to Lake Hartwell1991-11-26026 November 1991 PNO-II-91-074B:on 911123,unit Remained in Cold Shutdown,Per Declaration of Alert at 0214 Due to Leak in Rcs.As of 911126,total of 7,800 Gallons of Treated Water Released from Plant to Lake Hartwell ML20134D2581991-06-0404 June 1991 Notice of Violation from Insp on 910312-15.Violations Noted:Station Was Not Maintained According to Main Procedure MP/0/A/1800/105,Section 6.5,which Clearly Identified That Flange Was to Be Installed on Valve 3LP19 IR 05000269/19910081991-04-10010 April 1991 Insp Repts 50-269/91-08,50-270/91-08 & 50-287/91-08 on 910312-15.violations Noted.Major Areas Inspected:Maint, Control Room Operation,Planning & Scheduling Activities, Training & Procedures,Plant Physical Condition & Mgmt PNO-II-90-070, on 901108,unit Commenced Controlled Shutdown from 60% Power Due to Tube Leak in Steam Generator a1990-11-0808 November 1990 PNO-II-90-070:on 901108,unit Commenced Controlled Shutdown from 60% Power Due to Tube Leak in Steam Generator a IR 05000269/19900321990-11-0505 November 1990 Partially Withheld Insp Repts 50-269/90-32,50-270/90-32 & 50-287/90-32 on 901015-19.No Violations Noted.Major Areas Inspected:Physical Security Program Plans,Mgt Support, Security Program Plans & Protected & Vital Area Barriers IR 05000269/19900241990-10-0202 October 1990 SALP Repts 50-269/90-24,50-270/90-24,50-287/90-24 & 72-0004/90-24 for Feb 1989 - Jul 1990 IR 05000269/19900221990-07-24024 July 1990 Partially Withheld Safeguard Insp Repts 50-269/90-22, 5-270/90-22 & 50-287/90-22 on 900625-29.No Violations or Deviation Noted.Major Areas Inspected:Core Insp Program for Power Reactors & Safeguards Contingency Plan Implementation IR 05000269/19900181990-06-21021 June 1990 Partially Withheld Insp Repts 50-269/90-18,50-270/90-18 & 50-287/90-18 on 900604-08 (Ref 10CFR2.790 & 73.21).No Violations Noted.Major Areas Inspected:Security Program Audit,Detection & Assessment Aids & Key Control IR 05000269/19890201989-07-25025 July 1989 Partially Withheld Insp Repts 50-269/89-20,50-270/89-20 & 50-287/89-20 on 890626-30 (Ref 10CFR2.790.(d) & 73.21). Violations Noted.Major Areas Inspected:Physical Security Program for Power Reactors & Security Audit IR 05000269/19890101989-05-19019 May 1989 Partially Withheld Insp Repts 50-269/89-10,50-270/89-10 & 50-287/89-10 on 890410-14 (Ref 10CFR2.790 & 73.21). Violations Noted.Major Areas Inspected:Mgt Support,Security Program Plans & Audits & Protected & Vital Area Barriers IR 05000269/19890091989-04-10010 April 1989 Insp Repts 50-269/89-09,50-270/89-09 & 50-287/89-09 on 890306-10.No Violations Noted.Weaknesses Noted Re Data Base Used to Prepare computer-generated Work Requests.Major Areas Inspected:Design Control,Mods & Open Items IR 05000269/19890071989-03-10010 March 1989 Insp Repts 50-269/89-07,50-270/89-07 & 50-287/89-07 on 890213-17.Deviation Noted.Major Areas Inspected:Conformance to Reg Guide 1.97 Re Instrumentation for light-water-cooled Plants to Assess Conditions During & Following Accident IR 05000269/19880051988-03-21021 March 1988 Insp Repts 50-269/88-05,50-270/88-05 & 50-287/88-05 on 880217-0316.No Violations Noted.Major Areas Inspected:Maint, Operations,Surveillance,Physical Security & Design Changes PNO-II-88-013, on 880211,two Workers Slightly Contaminated W/ Radioactive Water.Caused by Approx 1,000 Gallon Leak of Radioactive Water Occurring During Maint on Valve.Workers Showered to Remove Contamination1988-02-12012 February 1988 PNO-II-88-013:on 880211,two Workers Slightly Contaminated W/ Radioactive Water.Caused by Approx 1,000 Gallon Leak of Radioactive Water Occurring During Maint on Valve.Workers Showered to Remove Contamination ML20237B2261987-12-15015 December 1987 EN-87-017A:informs That 870309 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000 Withdrawn Due to Determination That Violation Did Not Occur. Violation Based on Failure of Emergency Feedwater Pumps ML20235T5821987-09-18018 September 1987 Exam Rept 50-269/OL-87-02 on 870713-23.Exam Results:Seven of Ten Reactor Operator (RO) & Eight of Nine Senior Reactor Operator (SRO) Candidates Passed Written Exam.All RO & SRO Candidates Passed Operating Exam ML20238F7081987-09-0909 September 1987 Exam Rept 50-269/OL-87-01 for Units 1,2 & 3 on 870713-17. Exam results:7 of 10 Reactor Operators & 3 of 6 Senior Reactor Operators Passed ML20236E5111987-07-14014 July 1987 EN-86-056:on 870717,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000 Will Be Issued to Licensee.Action Based on Failure to Properly Implement Startup Procedure Causing Trains to Fail IR 05000269/19870091987-03-17017 March 1987 Insp Repts 50-269/87-09,50-270/87-09 & 50-287/87-09 on 870209-13.No Violations Noted.Major Areas Inspected:Onsite Review of Liquid & Gaseous Radwaste Programs & Review of TMI Action Items II.B.3 & II.F.1.2 IR 05000269/19870101987-03-17017 March 1987 Insp Repts 50-269/87-10,50-270/87-10 & 50-287/87-10 on 870210-0309.No Violations or Deviations Noted.Major Areas Inspected:Areas of Operations,Surveillance,Maint,Followup of Events & Verification of ESF Lineups ML20207T5431987-03-12012 March 1987 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000.Noncompliance Noted:Measures Not Established to Assure That Regulatory Requirements & Design Bases Correctly Translated Into Specs,Drawings & Procedures IR 05000269/19870061987-03-0909 March 1987 Insp Repts 50-269/87-06,50-270/87-06 & 50-287/87-06 on 870126-30.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp,Ongoing Repairs in Reactor Coolant Pumps & Maint & Welding Activities ML20207R4851987-03-0909 March 1987 EN-87-017:on 870312,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000 Will Be Issued to Util Based on Failure to Provide Adequate Design Control to Ensure Emergency Feedwater Pump Operability IR 05000269/19870041987-02-17017 February 1987 Insp Repts 50-269/87-04,50-270/87-04 & 50-287/87-04 on 870113-0209.No Violation or Deviation Noted.Major Areas Inspected:Operations,Surveillance,Maint,Verification of ESF Linups,Followup of Events & Shutdown Work in Progress IR 05000269/19870021987-02-11011 February 1987 Partially Withheld Insp Repts 50-269/87-02,50-270/87-02 & 50-287/87-02 on 870126-30 (Ref 10CFR2.790).Violation Noted Re Inadequate App R Circuit Analysis ML20211A4991987-02-11011 February 1987 Notice of Violation from Insps on 870112-16 IR 05000269/19870031987-02-10010 February 1987 Insp Repts 50-269/87-03,50-270/87-03 & 50-287/87-03 on 870112-16.Violation Noted:Failure to Adequately Evaluate Radiological Hazards ML20210U3211987-02-0505 February 1987 Notice of Violation from Insp on 861015-1110.Violation Noted:For Periods in 1978,1981 & 1986 When Lake Keowee Elevation Less than 792 Ft,Emergency Condenser Cooling Water Sys Inoperable & Unable to Provide Sustained Siphon Flow IR 05000269/19870071987-02-0505 February 1987 Enforcement Conference Repts 50-269/87-07,50-270/87-07 & 50-287/87-07 on 861222.Major Areas Discussed:Sequence of Events & Corrective Actions Re Emergency Condenser Circulating Water Sys Degradation IR 05000269/19870081987-02-0505 February 1987 Enforcement Conference Repts 50-269/87-08,50-270/87-08 & 50-287/87-08 on 861222.Major Areas Discussed:Safety Sys Functional Insp & Associated Safety Implications IR 05000269/19860341987-02-0505 February 1987 Corrected Insp Repts 50-269/86-34,50-270/86-34 & 50-287/86-34 on 861111-870112.Insp Erroneously Reported as Having Been Conducted on 861111-0112 ML20211A0871987-02-0303 February 1987 Notice of Violation from Insp on 870105-08 IR 05000269/19870011987-01-30030 January 1987 Insp Repts 50-269/87-01,50-270/87-01 & 50-287/87-01 on 870105-08.Violation Noted:Failure to Provide Procedures W/Appropriate Qualitative or Quantitative Acceptance Criteria for Activities Important to Safety ML20211A0061987-01-23023 January 1987 Insp Repts 50-269/86-34,50-270/86-34 & 50-287/86-34 on 861111-870112.No Violations or Deviations Noted.Major Areas Inspected:Operations,Surveillance,Maint,Verification of ESF Lineups & Emergency Drills ML20210U9961987-01-22022 January 1987 Exam Rept 50-269/OL-86-03 on 861215.Exam Results:Two Reactor Operator Candidates Passed Written Reexam.Written Exam Questions & Answer Key Encl IR 05000269/19860351987-01-0707 January 1987 Insp Repts 50-269/86-35,50-270/86-35 & 50-287/86-35 on 861208-12.No Violations or Deviations Noted.Major Areas Inspected:Radiation Protection Program,Including Review of Organization & Mgt of Health Physics Staff ML20212F5511986-12-24024 December 1986 Notice of Violation from Insp on 861103-12 PNO-II-86-092, on 861218,licensee Shut Down Unit to Begin Scheduled Refueling Outage 6 Wks Early.Caused by Excessive Vibrations in Reactor Coolant Pump 3B2.During Outage,Reactor Coolant Pumps 3B1,3B2 & 3A1 Will Be Modified1986-12-18018 December 1986 PNO-II-86-092:on 861218,licensee Shut Down Unit to Begin Scheduled Refueling Outage 6 Wks Early.Caused by Excessive Vibrations in Reactor Coolant Pump 3B2.During Outage,Reactor Coolant Pumps 3B1,3B2 & 3A1 Will Be Modified IR 05000269/19860321986-12-10010 December 1986 Insp Repts 50-413/86-44,50-414/86-47,50-369/86-32, 50-370/86-32,50-269/86-32,50-270/86-32 & 50-287/86-32 on 861103-12.Violations Noted:Failure to Follow Procedures for Radiological Sample Analyses & Inadequate Surveys IR 05000269/19860281986-11-0303 November 1986 Partially Withheld Physical Security Insp Repts 50-269/86-28,50-270/86-28 & 50-287/86-28 on 861014-17 (Ref 10CFR2.790 & 73.21).Violation Noted:Inadequate Protected Area Barrier 1997-09-26
[Table view] |
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NOTICE OF VIOLATION Duke Power Company Docket Nos. 50-269, 50-270, 50-287 Oconee Nuclear Station License Nos. DPR-38, DPR-47, DPR-55 Units 1, 2, and 3 EA 91-049 During an NRC inspection conducted on March 12 - 15, 1991, violations of NRC requirements were identified. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1991) the violations are listed below:
A. Technical Specification 6.4.1 requires that the station be operated and maintained in accordance with approved procedures. It also states that written procedures with appropriate check-off lists and instructions be provided for preventive or corrective maintenance which could affect nuclear safety or radiation exposure to personnel.
Maintenance Procedure MP/0/A/1800/105, Reactor Building Emergency Sump Low Pressure Injection Suction Line Flange Installation, Removal and Screen Inspection, approved on August 2,1990, provides guidance for the installation and removal of the Reactor Building Emergency Sump Low Pressure Injection suction line flange and sump screen inspection.
Sections 6.5 and 11.2 of this procedure contains steps for identifying the sump line and installing the blank flange for testing purposes.
Contrary to the above, on February 22, 1991, the station was not maintained in accordance with approved procedures in that Maintenance Procedure MP/0/A/1800/105, Section 6.5, which clearly identified that a flange was to be installed on valve 3LP-19, was not followed in that personnel installed a flange on valve 3LP-20 and subsequently signed off the procedure step and then performed an independent verification that the correct installation had been performed in accordance with Steps .11.2.1, 11.2.5-11.2.10 of the procedure.
B. Technical Specification 6.4.1 requires that the station be operated and maintained in accordance with approved procedures. It also states that written-procedures with appropriate check-off lists and instructions be -
provided for preventive or corrective maintenance which could affect j nuclear safety or radiation exposure to personnel.
Procedure PT/3/A/203/04, Low Pressure Injection System Leakage, approved on March 28, 1939, contains guidance for periodically testing the Low Pressure Injection System outside containment and for verifying that i valves 3LP-19 and 3LP-20 can be manually opened. Enclosure 13.2 of the procedure provides instructions for leak test of the emergency sump line ;
to valve 3LP-19 during a unit outage. !
Contrary to the above, on February 23, 1991, steps contained in the enclosure to the procedure for valve 3LP-19 were verified as having been I completed, when in fact, a blank flange had been installed on valve 3LP-20 i and that line had been filled and hydrostatically tested. j 1
9610210053 910604
{DR ADOCK 05000269 )
PDR l
1
. l Notice of Violation C. 10 CFR 50, Appendix B, Criterion V, and the licensee's accepted Quality Assurance Program (Duke Power Company Topical Report, Quality Assurance Program, Duke-1-A), Section 17.2.5, collectively require that activities affecting quality be prescribed by procedures of a type appropriate to the circumstances and that such activities be accomplished in accordance with these procedures. Oconee Nuclear Station Operations Management Procedure (OMP) 4-5, Station Labeling and Control Board Conventions, Revision 3, contains standards for the development, approval and installation of plant equipment labels.
Contrary to the above, on February 22, 1991, a non-standard label containing erroneous information was used by maintenance personnel during performance of quality-related activities. The non-standard label was not developed, approved or installed in accordance with OMP 4-5.
Violations A, B, and C have been categorized in the aggregate as a Severity Level III problem (Supplement 1).
Pursuant to the provisions of 10 CFR 2.201, Duke Power Company is hereby required to submit a written statement or explanation to the U. S. Nuclear Regulatory Comission, ATTN: Document Control Desk, Washington, D.C. 20555 with a copy to the Regional Administrator, U. S. Nuclear Regulatory Commission, Region II,101 Marietta Street, N.W., Suite 2900, Atlanta, GA 30323, and a copy to the U. S. Nuclear Regulatory Commission Senior Resident Inspector at the Oconee Nuclear Station, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be clearly marked as a " Reply to a Notice of Violation" and should include for cach violation: (1) the reason for the violation, or, if contested, the basis for disputing the violation, (2) the corrective steps that have been taken and the results achieved, (3) the corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achieved. If an adequate reply is not received within the time specified in this Notice, an order may be issued to show cause why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time. Under the authority of Section 182 of the Act, 42 U.S.C. 2232, this response shall be submitted under oath or affirmation. -
FOR THE NUCLEAR REGULATORY COMMISSION Stewart D. Ebneter Regional Administrator Dated at Atlanta, Georgia this # 4 day of June 1991