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PNO-II-97-065, on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG29 December 1997PNO-II-97-065:on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG
PNO-II-97-034, on 970613,extended Shutdown to Meet CAL 2-97-03 Commitments to Shutdown Unit 1 No Later than 970614 & to Implement Actions Re HPI Sys.Nrc Resident Inspector Will Followup on Unit 1 Shutdown & Recovery Activities13 June 1997PNO-II-97-034:on 970613,extended Shutdown to Meet CAL 2-97-03 Commitments to Shutdown Unit 1 No Later than 970614 & to Implement Actions Re HPI Sys.Nrc Resident Inspector Will Followup on Unit 1 Shutdown & Recovery Activities
PNO-II-93-039, on 930823,reactor Trip Occurred Due to Loss of Power to Vital Panelboard.Investigation Team Dispatched to Site to Review Root Cause & Plant Response.State & Local Authorities Notified24 August 1993PNO-II-93-039:on 930823,reactor Trip Occurred Due to Loss of Power to Vital Panelboard.Investigation Team Dispatched to Site to Review Root Cause & Plant Response.State & Local Authorities Notified
PNO-II-92-070, on 921019,several Circuit Breakers Failed in 230KV Switchyard to Open Position for Unknown Reasons. Licensee Has Inititated Investigation to Review Event to Determine Cause & Determine Why Certain Equipment Failed20 October 1992PNO-II-92-070:on 921019,several Circuit Breakers Failed in 230KV Switchyard to Open Position for Unknown Reasons. Licensee Has Inititated Investigation to Review Event to Determine Cause & Determine Why Certain Equipment Failed
PNO-II-91-074B, on 911123,unit Remained in Cold Shutdown,Per Declaration of Alert at 0214 Due to Leak in Rcs.As of 911126,total of 7,800 Gallons of Treated Water Released from Plant to Lake Hartwell26 November 1991PNO-II-91-074B:on 911123,unit Remained in Cold Shutdown,Per Declaration of Alert at 0214 Due to Leak in Rcs.As of 911126,total of 7,800 Gallons of Treated Water Released from Plant to Lake Hartwell
PNO-II-90-070, on 901108,unit Commenced Controlled Shutdown from 60% Power Due to Tube Leak in Steam Generator a8 November 1990PNO-II-90-070:on 901108,unit Commenced Controlled Shutdown from 60% Power Due to Tube Leak in Steam Generator a
PNO-II-88-013, on 880211,two Workers Slightly Contaminated W/ Radioactive Water.Caused by Approx 1,000 Gallon Leak of Radioactive Water Occurring During Maint on Valve.Workers Showered to Remove Contamination12 February 1988PNO-II-88-013:on 880211,two Workers Slightly Contaminated W/ Radioactive Water.Caused by Approx 1,000 Gallon Leak of Radioactive Water Occurring During Maint on Valve.Workers Showered to Remove Contamination
PNO-II-86-092, on 861218,licensee Shut Down Unit to Begin Scheduled Refueling Outage 6 Wks Early.Caused by Excessive Vibrations in Reactor Coolant Pump 3B2.During Outage,Reactor Coolant Pumps 3B1,3B2 & 3A1 Will Be Modified18 December 1986PNO-II-86-092:on 861218,licensee Shut Down Unit to Begin Scheduled Refueling Outage 6 Wks Early.Caused by Excessive Vibrations in Reactor Coolant Pump 3B2.During Outage,Reactor Coolant Pumps 3B1,3B2 & 3A1 Will Be Modified
PNO-II-86-078, on 861021,2 Gallons of Hydrazine Spilled in Turbine Bldg.Caused by Leak in Deionized Water Mixing Valve Overflowing Mix Tank.Spill Cleaned Up22 October 1986PNO-II-86-078:on 861021,2 Gallons of Hydrazine Spilled in Turbine Bldg.Caused by Leak in Deionized Water Mixing Valve Overflowing Mix Tank.Spill Cleaned Up
PNO-II-86-069, on 861002,Units 1 & 2 Shut Down Due to Loss of Low Pressure Svc Water Pump Suction After Surveillance Test. Caused by Air Leakage in Pump Flange Seals.Leakage Areas Wrapped.All Units Shutdown Until Exact Cause Determined3 October 1986PNO-II-86-069:on 861002,Units 1 & 2 Shut Down Due to Loss of Low Pressure Svc Water Pump Suction After Surveillance Test. Caused by Air Leakage in Pump Flange Seals.Leakage Areas Wrapped.All Units Shutdown Until Exact Cause DeterminedUltimate heat sink
PNO-II-86-055, on 860806,plant Began Shutdown Due to Leak in Steam Generator a Tube Calculated at 0.26 Gallons Per Minute.Shutdown Expected to Last 10 Days7 August 1986PNO-II-86-055:on 860806,plant Began Shutdown Due to Leak in Steam Generator a Tube Calculated at 0.26 Gallons Per Minute.Shutdown Expected to Last 10 Days
PNO-II-86-036, on 860515,during Power Escalation Tests at 100% Power,Steam Generator Tube Leak Detected.Unit Out of Svc for 10 Days to Repair Leak19 May 1986PNO-II-86-036:on 860515,during Power Escalation Tests at 100% Power,Steam Generator Tube Leak Detected.Unit Out of Svc for 10 Days to Repair Leak
PNO-II-86-014, on 860213,mild Earthquake Felt at Site.Plant Turbine & Auxiliary Bldgs Surveyed & No Damage Found. Preliminary Review of Detection Equipment at Site Indicated No Evidence of Ground Movement or Tremor13 February 1986PNO-II-86-014:on 860213,mild Earthquake Felt at Site.Plant Turbine & Auxiliary Bldgs Surveyed & No Damage Found. Preliminary Review of Detection Equipment at Site Indicated No Evidence of Ground Movement or TremorEarthquake
PNO-II-85-111, on 851124,unscheduled Shutdown Greater than 48 H Anticipated.Caused by Failure of High Pressure Turbine Bearing.Outage of at Least 8 Days Expected for Evaluation & Repairs25 November 1985PNO-II-85-111:on 851124,unscheduled Shutdown Greater than 48 H Anticipated.Caused by Failure of High Pressure Turbine Bearing.Outage of at Least 8 Days Expected for Evaluation & Repairs
PNO-II-85-107, on 851107,plant Taken out-of-svc After Verification of Turbine High Bearing Temp.Caused by Main Turbine Bearing Failure.Plant Expected to Be Shut Down for 5 to 14 Days for Repairs7 November 1985PNO-II-85-107:on 851107,plant Taken out-of-svc After Verification of Turbine High Bearing Temp.Caused by Main Turbine Bearing Failure.Plant Expected to Be Shut Down for 5 to 14 Days for Repairs
PNO-II-85-094, on 851007,unit Shut Down Due to Steam Generator Tube Leak.Leakage Amounted to 0.15 Gallon Per Minute & Increasing.Generator Isolated.Shutdown Expected for 10-12 Days8 October 1985PNO-II-85-094:on 851007,unit Shut Down Due to Steam Generator Tube Leak.Leakage Amounted to 0.15 Gallon Per Minute & Increasing.Generator Isolated.Shutdown Expected for 10-12 Days
PNO-II-85-068, on 850721,two Threatening Telecons Received by Switchboard & Another Call Received on Telephone Answering Machine in Ofc of NRC Resident Inspector.Security Contingency Plan Implemented & Agencies Informed22 July 1985PNO-II-85-068:on 850721,two Threatening Telecons Received by Switchboard & Another Call Received on Telephone Answering Machine in Ofc of NRC Resident Inspector.Security Contingency Plan Implemented & Agencies Informed
PNO-II-85-065, on 850708,routine Receipt Survey Identified Four Smears on Exterior of Empty NAC-1 Fuel Shipping Cask from Nuclear Assurance Corp in Excess of Max Permissible Limits.Measured Levels Posed No Threat to Public Safety9 July 1985PNO-II-85-065:on 850708,routine Receipt Survey Identified Four Smears on Exterior of Empty NAC-1 Fuel Shipping Cask from Nuclear Assurance Corp in Excess of Max Permissible Limits.Measured Levels Posed No Threat to Public SafetyExclusive Use
PNO-II-85-058, on 850607,licensee Reported That Individual Received Radiation Overdose to Small Area of Skin on Underarm.Caused by Particle Transfer from Protective Clothing.Person Decontaminated7 June 1985PNO-II-85-058:on 850607,licensee Reported That Individual Received Radiation Overdose to Small Area of Skin on Underarm.Caused by Particle Transfer from Protective Clothing.Person DecontaminatedOverdose
PNO-II-85-043, on 850425,most Control Room Annunciators Lost Due to Failure of Inverter Power Supply.Possibly Caused by Blown Fuse.One Feedwater Pump Restored to Operation25 April 1985PNO-II-85-043:on 850425,most Control Room Annunciators Lost Due to Failure of Inverter Power Supply.Possibly Caused by Blown Fuse.One Feedwater Pump Restored to Operation
ML20054L52129 June 1982Updated PNO-II-82-072A:on 820628,break Occurred in Outside Radius of Elbow 24-inch Line Which Branches Off 42-inch High Pressure Turbine Exhaust.Apparently Caused by Thinning from Steam Erosion
PNO-II-82-072, on 820628,at 95% Power,High Pressure Turbine Extraction Steam Line Break Resulted in Release of Steam to Turbine Bldg Basement.Three Workers Reported Injured by Steam.Reactor Manually Shut Down & Placed in Hot Standby28 June 1982PNO-II-82-072:on 820628,at 95% Power,High Pressure Turbine Extraction Steam Line Break Resulted in Release of Steam to Turbine Bldg Basement.Three Workers Reported Injured by Steam.Reactor Manually Shut Down & Placed in Hot Standby
PNO-II-82-065, visual & Ultrasonic Exams Revealed Cracks in 51 of 96 Thermal Shield Bolts.Removal of Bolts & Associated Locking Clips Revealed 19 of 27 Bolt Heads Broken.Bolts Will Be Replaced W/Stud & Nut Assemblies11 June 1982PNO-II-82-065:visual & Ultrasonic Exams Revealed Cracks in 51 of 96 Thermal Shield Bolts.Removal of Bolts & Associated Locking Clips Revealed 19 of 27 Bolt Heads Broken.Bolts Will Be Replaced W/Stud & Nut Assemblies
PNO-II-81-002, on 810107,two of Three Individuals Found to Have Nasal Contamination (3200 Dpm Max) Following Maint on Control Rod Drive Mechanisms in Reactor Bldg.Workers Nostrils Decontaminated.Whole Body Counts Performed7 January 1981PNO-II-81-002:on 810107,two of Three Individuals Found to Have Nasal Contamination (3200 Dpm Max) Following Maint on Control Rod Drive Mechanisms in Reactor Bldg.Workers Nostrils Decontaminated.Whole Body Counts Performed
PNO-II-80-150, on 801013,during Routine Check of Unit 2 Containment Purge Valve 5,purge Path Opened to Environ for 46 S.Caused by Failure to Follow Procedures in Proper Sequence.No Tech Spec Limits Exceeded.State of Sc Informed14 October 1980PNO-II-80-150:on 801013,during Routine Check of Unit 2 Containment Purge Valve 5,purge Path Opened to Environ for 46 S.Caused by Failure to Follow Procedures in Proper Sequence.No Tech Spec Limits Exceeded.State of Sc Informed
ML20249A2058 November 1978PNS-78-054:on 781106,NRC Region II Received Telephone Call from Security Guard Re Security Guard Training at Oconee.On 781107,NRC Investigators Met W/Group of Former & Present Guards Who Alleged Inadequate Training.Media Informed
ML20216J5884 August 1978PNO-78-141:on 780804,licensee Reported That Chemical Anaylsis of Reactor Vessel Weld Matl Performed by B&W Revealed That Silicon & Nickel Content Differed from That Specified
ML20216J6074 August 1978PNO-78-140:on 780803,employee at Plant Passed Out from Heat Exhaustion After Exiting Unit 1 Containment.Worker Was Treated,Released & Returned to Work Later That Day.No Injury Due to Radiation or Radioactive Contamination Occurred
ML20248H8615 May 1978PNO-78-102:on 780504,while RCS Was Open to Atmosphere, 50,000 Gallons of Reactor Coolant Overflowed Onto Containment Building Floor.Licensee Reported No Release of Radioactivity.State of South Carolina Notified
ML20248H61124 April 1978PN0-78-090:on 980421,Unit 1 Shutdown Commenced Due to SG Tube Leak.Unit 1 Will Be Placed in Cold Shutdown Condition, Portion of RCS Drained & SG Leak Tested to Identify Leaking Tubes for Repair.Estimated Duration of 2 Weeks for Shutdown
ML20248L02920 April 1978PNO-78-079B:supplements PNO 78-79A Dtd 780414.Informs That Addl Analyses Being Conducted by B&W.Licensee Reported That Operators Have Been Stationed at HPI Crossover Piping to Promptly Realign Sys for 2 Flow Paths Upon Break Detection
ML20248K98414 April 1978PNO-78-079A:supplements & Corrects Preliminary Info Provided in PNO-78-79 .Reanalysis Assumed Pipe Break of .04 Square Feet in RCP Discharge Piping.Region II Received Updated Info on 980413 & State of South Carolina Notified
ML20248K00913 April 1978PNO-78-079:licensee Reported That B&W Identified Error in Safety Analysis for Small Break in Rcs.Original Safety Analysis Was Done W/Small Break Occurring on Pump Discharge Line.State of Sc Notified
ML20207G4185 December 1977PNO-77-217:on 771205,following Refueling of Unit 3 & During Startup Physics Testing of Reloaded Core on 771204,core Power Distribution Measurements Revealed Seven Percent Flux Tilt at twenty-five Percent Power
ML20207G8134 November 1977PNO-77-193:on 771103,due to an Apparent SG Tube Leak of Approx 1.0 Gallon Per Minute (Gpm) Unit Was Shutdown
ML20207G63525 October 1977PNO-77-189:on 771016,following Refueling of Unit 1 & During Startup Physics Testing of Reloaded Core,Measured Values for Ejected Rod Worth Showed an Unexpected Reduction from Predicted Values
ML20151X70811 October 1977PNO-77-178:on 771007,unit Shutdown Commenced Due to SG Tube Leak of Approx 0.2 Gpm.Unit to Be Placed in Cold Shutdown for Approx 2 Wks While Repairs Conducted.Press & State of Sc Notified
ML20151X4151 September 1977PNO-77-152:film Badge Dosimeters Provided & Used by Five Contract Workers from Todd Shipyards,Galveston,Tx at Oconee Nuclear Station Indicated High Exposures Ranging from 1.3 Rems to 55 Rems
ML20151Y16315 July 1977PNO-77-129:on 770714,Unit Shutdown Was Commenced Due to Apparent SG Tube Leak.Unit Will Be Placed in Cold Shutdown Condition,Portion of RCS Will Be Drained & SG Will Be Leak Tested to Identify Leaking Tubes for Repair
ML20151V20512 May 1977PNO-77-083:on 770511,unplanned Release of Radioactivity in Liquid Occurred.Plant Personnel Investigating to Determine Cause.Monitoring of Turbine Bldg Sump & Yard Drainage Sys Continuing
ML20236K9342 February 1977PNO-77-019:on 770117,during SG Repair Activities,About 8,000 Gallons of Secondary Sys Water Was Inadvertently Released to Turbine Building Sumps
ML20236X03723 December 1975PN-75-155:on 751223,licensee Called Region II to Rept That Telephone Call Received from Man in Spartanburg,Sc Re Bomb Placed in Plant
ML20236U22513 June 1975PN-75-036:on 750613,DPC Notified Region II That Following Turbine Trip,Primary Sys Pressure Increased Where Primary Sys Electromatic Rv Opened to Reduce Pressure.Rv Stuck in Open Position & Pressure Reduced in 30 Minutes