ML20205N688

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Results of Foliar Survey of LaSalle County Generating Station for Rime Ice Deposition Damage
ML20205N688
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 01/16/1986
From: Jacobsen B
B.J. JACOBSEN, PHD
To:
Shared Package
ML20205N355 List:
References
0134H, 134H, NUDOCS 8605020257
Download: ML20205N688 (9)


Text

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Attachment 5

_, Page 1 of 4 RESULTS CP FOLIAR SURVEY OF TEI LASALLE COUNTY G1DIERATING STATION FCR RIME ICE DEPOSITION DAMAGE Prepared for commonwealth Edison Company -

a by Barry J. Jacobsen, PhD '

860Sog{h $

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Attachment 5 Page 2 of 4 l

7egetation in the vicinity of the LaSalle County Generating Station was surveyed for damage caused by rise ice deposition during the winter of 1984-85 This survey was done in accordance with section 4-2-2(d) of the LaSalle County Station Dtvironmental Protection Plan on the 15th of May, 1985 with the assistance of Mr. B.B. Barriskaan of the Commonwealth Edison Company and is the second survey of this site done by Barry J. Jacobsen, Ph.D.

Summaries of the 4th quarter of 1984 and lat quarter of 1985 of the Fog and Rime Ice Monitoring Program for the LcSalle Station were utilised to identify areas of most likely damage. The survey area is shown in Figure 1 (attached). Also shown in this

' figure are specifie sites sentioned in this report. The survey area was sufficiently large so that similar plants could be observed in areas reported to be with and without rise ice.

Site #1 located around the cooling water discharge was the l site where rise ice was reported acet frequently during January j of 1985 Cottonwood, willow, autumn olive and sweet olover observed at this site did not show evidence of lee damage. 1 j

However, willows located north of the cooling water disoharge did '

show more winter injury and sanker disease (Venturia and cytospora) than other willows in the survey area. Winter injury was dias * -

l nosed based on tip diebeek and one sided osabium noorosis and bud death. This winter injury is thought to be due to the vara discharge water delaying the vernalisation process. This delay

  • i in vernalisation does not allow the plant tissues to harden off

! enough to prevent freezing injury when extreme cold occurs. The winter injury noted was relatively stnor in nature. Willows growing 25-50 yards north of the cooling wazar disonarse also had wood borer damage.

Autumn olive plantings in this area also displayed. some dieteck.

However, the distribution and type of dieback is suggestive of prob-less relating to transplanting and plant establishment.

Sweet olover growing in this area showed no evidense of seethering such as would be expeeted from ice damage.

Site #2 located to the west of the ecoling water discharge had apple and oak. trees.uhich showed winter damage. This damage.is thought 'to re% ate.te the venalization problem mentioned above and not ice daange.;

Dogwood standings at this site showed evidence of transplant damage again in 1983, although most plants show evidense of recovery.

Sweet elover and erown vetah growing at this site showed no signs of ice smothering.

Site #1 was characteristie of crown vetch growing on the banks of the pond containment dike. Growth was exoellent and there was little sign of the Volutella canker disease seen in the 1984 survey.

Site #4 was contiguous with observation site #7 used in the fog and rise ice monitoring reports. Dieback was noted only in a row of old Osage orange trees growing adjacent to a pasture.

1

Attachment 5

, Page 3 of 4 1985 Folear survey Page 2 Diebeek was not characteristis of ice or winter damage. Cieback was characteristia of root damage and/or canker or decay problems.

Site #5 was loested between fog and rise lee observation sites M and M. A new home with new landscape tree plantings was located at this site. These plantings coeurred in 1984 and did not show los or winter damage.

site M was located at 0.7 miles west of fog and rise toe observation site M. An old planting of hard amples showed evidsnee of diebeek relating to decay at this abandoned building site. There was no evidense of ice damage.

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Cont'AM.11_Q_n 31ae loing was not a factor in vegatation injury in and around the LaSalle County Generating Station during the winter of 1984-85 I Dieback associated with delayed vernalization near the cooling water '

dischstge site een be assosisted with plant operation. However, this damage is minor and is limited only to obliews which of ten show - i winter injury. -

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rr DOCUMENT ID 0134h

e 5.4.2 Nonroutine Reports NONE M ENT ID Ol34h

o ATTAC19 TENT 6 Sunusary of NPDES noncompliances for 1985. These have been previously reported to'the NRC at the time the report was submitted to the State of Illinois. These are not EPP noncompliances.

DOC 13 TENT ID 0134h

c a-e LASALLE COUNTY STATION NPDES NON-COMPLIANCES 1985 DVR NUMBER DATE NON-COMPLIANCE CORRECTIVE ACTION 1-1-85 10 Jan 85 001 (a) Demineralizer Regenerant

-Discharge was' discontinued following confirmation Wastes pH(1) of the.9.2 pH result.

1-1-85-57 27 Feb 85 001 Cooling Pond Blowdown Total None taken.

Iron (1) 1-1-85-66 13 Mar 85 001 (b) Sewage Treatment Plant Efforts made to sample Sewage Treatment Plant Effluent Fecal Coliform (2) effluent after more contact time with chlorine.

1-1-85-88 .4 Apr 85 001 Cooling Pond Blowdown Total Requesting NPDES permit modification.

Iron (4) ,

1-1-85-97 26 Apr 85 001 Cooling Pond Blowdown Total Requesting NPDES permit modification.

1 Iron (2) 1-1-85-121 3 Jun 85 001 (c) Wastewater Treatment Facility Discharge was isolated. Clearwell pumped back j

pH (1) to equalization tank and neutralized.

1-1-85-122 4 Jun 85 001 (a) Regenerative Wastes Solution Discharge was isolated. Possible inadequate Discharge Tank pH and Total Suspended mixing due to low flow through transfer pumps solids-(2). to be investigated.

1-1-85-143 01 Jul 85 001 (a) Regenerative Wastes Solution OWM03T and OWM12T Tanks were drained, inspected, Discharge Tank TSS (1) and cleaned since solids had accumulated in the tanks.

l 1-1-85-144 03 Jul 85 001 (c) Wastewater Treatment System Oil and Grease was pumped out of clarifiers, Effluent Oil and Grease (3) equalization tank, and oil separator pit. Oil absorbent booms in clearwell and effluent chamber were replaced.

001 (c) Wastewater Treatment Facility Discharge isolated. Media filter 'A' replaced.

1-1-85-160 29 Jul 85 l Total Suspended Solids and 011 and Oil pumped out of equalization tank, clarifiers, Grease (4) clearwell, and effluent compartment. Oil absorbent booms replaced. Polymer was replaced.

Inspection of oil trough..

DOCUMENT 0309h

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LASALill COUNTY STATION NPDES NON-COMPLIANCES *-

1985 DVR NUMBER DATE NON-COMPLIANCE CORRECTIVE ACTION 1-1-85-l~12 19 Sep 85 001(a) Demineralizer Regenerant Waste Composite sampler previously out of service has TSS (1) been repaired and put into use.

1-1-85-180 4 Oct 85 001 (c) Wastewater Treatment System Replaced oil booms in clarifier and eq. tank.

Effluent 011 and Grease (3) Media filter 'A' changed out on 25 Sep 85.

l 2 daily, 1 monthly. AIR's written to pump sludge out of oil separator and increase polymer concentration to equal vendor's recommendations.

1-1-85-185 11 OCT 85 001 (a) Demineralizer Regenerant Discharge at low flow rate as not to dislodge Wastes TSS (1) accumulated solids in low point of piping. Clean standstill acid sump and area around sump.

1-1-85-189 16 Oct 85 001 (c) Wastewater Treatment Anthracite coal added to media filter 'B' to bring System TSS (1) it to correct level on 18 Oct 85. Anionic polymer skid put back into service on 17 Oct 85.

Polymer manually mixed. Composite sampler has been reprogrammed to sample correct volume, 1-1-85-191 15 Oct 85 001 (c) Wastewater Treatment AIR written to identify source of oil and System 011 & Grease (1) correct problem. Effluent chamber boom removed and not replaced. AIR 373-200-85-18001 tracking new tube bundles for oil separator.

1-1-85-192 31 Oct 85 001 (a) Demineralizer Regenerant Discharge at low flowrate only. Caution card Wastes TSS (30-day avg)(1) hung on crosstie valve OWM213. Clean standstill acid sump and areas around sump.

1-1-85-193 31 Oct 85 001 (c) Wastewater Treatment Anthracite coal added to media filter 'B' to bring System TSS (30-day avg) (1) it to correct level on 18 Oct 85. Anionic polymer skid put back into service on 17 Oct 85.

Polymer manually mixed. Composite sampler has been reprogrammed to sample correct volume.

1-1-85-207 12 Nov 85 001 Cooling Pond Blowdown None taken (heavy rainfall).

Total Iron (2)

DOCUMENT 0309h

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