ML20132E384

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Insp Repts 50-324/85-16 & 50-325/85-16 on 850601-30. Violation Noted:Inadequate Surveillance Test Procedure for Refueling Hoist Slack Cable Interlock
ML20132E384
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 07/12/1985
From: Fredrickson P, Garner L, Hicks T, Ruland W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20132E361 List:
References
50-324-85-16, 50-325-85-16, NUDOCS 8508010799
Download: ML20132E384 (11)


See also: IR 05000324/1985016

Text

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                 o                                     UNITED STATES
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      y               j                          101 MARIETTA STREET.N.W.
      *               2                           ATL ANTA, GEORGI A 30323
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        Report Nos.: 50-325/85-16 and 50-324/85-16
        Licensee: Carolina Power and Light Company
                      P. O. Box 1551
                      Raleigh, NC 27602
        Docket Nos.:      50-325 and 50-324                         License Nos.: DPR-71 and DPR-62
        Facility Name: Brunswick 1 and 2
        Inspection Conducted: June 1-30, 1985
        Inspectors:       h[
                      W. H .' 'Rtil a n'd-
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                                                                                        Date Signed
                       L. W'.
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                               Garner
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                                                                                        Da'te Signed
                          dKAfrw/n &
                      T. E. Hicks                       d
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                                                                                        Date Signed
        Approved by:
                        P. E. Fredr1ckson, Sectio Chief
                                         ~
                                                                                        7MA[[I
                                                                                        Date Signed
                        Division of Reactor Projects
                                                         SUMMARY
        Scope: This routine safety inspection involved 300 inspector-hours on site in
        the areas of followup on previous enforcement matters, maintenance observation,
        surveillance observation, operational                 safety verification, onsite review
        committee, onsite Licensee Event Report review, followup on inspector identified
        and unresolved items, plant modifications, and refueling activities.
        Results: A violation was identified - inadequate surveillance test procedure for
        the refueling hoist slack cable interlock.
                         $$$          4
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                                      REPORT DETAILS
     1. Persons Contacted
        P. Howe, Vice President - Brunswick Nuclear Project
        C. Dietz, General Manager - Brunswick Nuclear Project
        T. Wyllie, Manager - Engineering and Construction
        G. Oliver, Manager - Site Planning and Control
        J. Holder, Manager - Outages
        E. Bishop, Assistant to General Manager
        L. Jones, Director - QA/QC
        M. Shealy, Acting Director - Training
        M. Jones, Acting Director - Onsite Nuclear Safety - BSEP
        J. Chase, Manager - Operations
        J. O'Sullivan, Manager - Maintenance
        G. Cheatham, Manager - Environmental and Radiation Control
        K. Enzor, Director - Regulatory Compliance
        B. Hinkley, Manager - Technical Support
        L. Boyer, Director - Administrative Support
        V. Wagoner, Director - IPBS/Long Range Planning
        C. Blackman, Superintendent - Operations
        J. Wilcox, Principal Engineer - Operations
        W. Hogle, Engineering Supervisor
        W. Tucker, Engineering Supervisor
        B. Wilson, Engineering Supervisor
        R. Creech, I&C/ Electrical Maintenance Supervisor (Unit 2)
        J. Moyer, I&C/ Electrical Maintenance Supervisor (Unit 1)
        R. Kitchen, Mechanical Maintenance Supervisor (Unit 2)
        R. Poulk, Senior NRC Regulatory Specialist
        D. Novotny, Senior Regulatory Specialist
        W. Dorman, QA - Supervisor
        W. Hatcher, Security Supervisor
        W. Murray, Senior Engineer - Nuclear Licensing Unit
     2. Exit Interview
        The inspection scope and findings were summarized on June 28, 1985, with the
        general manager.    A violation described in paragraph 5 was discussed in
        detail.    The licensee acknowledged the findings without exception. The
        licensee did not identify as proprietary any of the materials provided to or
        reviewed by'the inspectors during this inspection.
     3. Followup on Previous Enforcement Matters (92702)
        (0 pen) Violation 325, 324/82-10-02:     Failure to Implement Independent
        Verification per NUREG 0737 Item I.C.6. This item will remain open pending
        inspectors' review of the licensee's present implementation of I.C.6.

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      ,
             (Closed) Violation 325,324/84-35-01: Failure to Establish Adequate
             Implementing Procedure for Operating Procedure OP-32.
             (Closed) Violation 324/82-39-01: Procedure Does Not Contain Isolation Valve
             for Low Condenser Vacuum Instrument. The inspector verified that the
             subject valves are included in the current revision (No. 32) to OP-30. As
             part of the operating procedure rewrite program, th licensee verified or
             included as necessary similar instrument isolation valves. This program was
             completed in December 1983.
             (Closed) Violation 324/82-39-04:    Failure to Bypass Low Condenser Vacuum
             Above 500 psig.
             (Closed) Violation 324/82-39-03:    Failure to Follow Procedure EI-13, Mode
             Switch Not Locked.
             (Closed) Violation 325/83-30-01 and 324/83-30-01: Surveillance Test Method
             To Time Standby Gas Treatment System Inlet and Outlet Dampers Is Inadequate.
             The licensee's response, dated October 12, 1983, to the Notice of Violation
             committed to: (1) revise PT-15.7 to use MCC position indication or visual
             observation of valve travel, (2) revise OP-10 to provide a caution note that
             the control room position lights do not reflect actual valve position and
             such can be obtained from MCC and, (3) review to determine if similar
             conditions exist on other valves.
             The inspector verified that the current revisions, revision 14 to PT-15.7,
             revision 5 to Unit 1 OP-10 and revision 24 to Unit 2 OP-10 contain changes
             as committed.    The review disclosed no additional similar conditions on
             other valves.
             (Closed) Violation 325/82-10-05 and 324/82-10-05: Failure to Implement
             Maintenance Procedure MI3-3A34.    The licensee failed to perform corrective
             actions as described in their response (dated May 24,1982) to the Notice of
             Violation. Another. Notice of Violation was issued in report 325, 324/82-45.
             Corrective action will be inspected as part of the followup on the latter
             violation. This item is considered closed for administrative purposes.
             No violations or deviations were identified.
          4. Maintenance Observation (62703)
             The inspectors observed maintenance activities and reviewed records to
             verify that work was conducted in accordance with approved procedures,
             Technical Specifications, and applicable industry codes and standards. The
             inspectors also verified that: redundant components were operable;
             administrative controls were followed; tagouts were adequate; personnel were
             qualified; correct replacement parts were used; radiological controls were
             proper; fire protection was adequate; QC hold' points were adequate and
             observed; adequate post-maintenance testing was performed; and independent
             verification requirements were implemented. The inspectors independently
             verified that selected equipment was properly returned to service.
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             Outstanding work requests and authorizations (WR&A) were reviewed to ensure
             that the licensee gave priority to safety-related maintenance.
             The inspectors observed / reviewed portions of the following maintenance
             activities:
            Work Request and Authorization (WR&A) No.1-M-85-2109, IC Residual Heat
             Removal (RHR) Service Water Booster Pump, Damaged Bearing.
            WR&A No. 1-M-85-2199, 1C RHR Booster Pump High Vibration, High Bearing
             Temperature.
            WR&A No. 2-M-85-2384, Core Spary Minimum Flow Bypass Valve Repairs,
             2E21-F031A.
            WR&A No. 0-E-85-1793, Scram Solenoid Valve Replacement Unit 1.
             No violations or deviations were identified.
      5.     Surveillance Observation (61726)
             The inspectors observed surveillance testing required by Technical Specifi-
            cations. Through observation and record review, the inspectors verified
             that: tests conformed to Technical Specification requirements; administra-
             tive controls were followed; personnel were qualified; instrumentation was
            calibrated; and data was accurate and complete. The inspectors
             independently verified selected test results and proper return to service of
             equipment.
             The inspectors witnessed / reviewed portions of the following test activities:
           *1MST-RP622R, Main Steamline Isolation Valve Closure Channel Calibration.
             PT-12.3.1, Emergency Diesel Generator Annual Inspection.
            PT-12.4, Diesel Generator Alarms, Trips and Trip Bypass Test.
            PT-85-071, Special Procedure for Response Time for Relays E41A-K4 and
            E41A-K5.
            PT-12.20, No. 4 Diesel Generator Monthly Load Test.
         . IMST-RHR21R, Residual Heat Removal, Low Pressure Coolant Injection, Core
            Spray System, High Pressure Coolant Injection (HPCI) High Drywell Pressure
            Trip Unit Channel Calibration.
            PT-16.2-2, Primary Containment Volumetric Average Temperature, Rev.1.
           * Detailed Review
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     a. HPCI Response Time Testing
        On June 21, 1985, the Maintenance Surveillance Test (MST) procedure
        writing groups discovered a discrepancy in the current High Pressure
        Coolant Injection (HPCI) System initiation response time test,
        Periodic Test (PT) 45.3.4. This PT failed to adequately calculate the
        response time for the HPCI System initiation logic as required by
        Technical Specification 4.3.3.3.
        PT-45.3.4, HPCI initiation response time test was undergoing an upgrade
        process by the MST rewrite group (see LER 1-85-03). The procedure
        covered Technical Specification 4.3.3.3, which states that the
        Emergency Core Cooling System (ECCS) response time of each ECCS
        function shall be demonstrated to be within the required limits at
        least once per 18 months. The definition of ECCS response time is
        "that time interval from when the monitored parameter exceeds its ECCS
        actuation setpoint at the channel sensor until the ECCS equipment is
        capable of performing its safety function."
        The current test method adds two partial response times to obtain the
        total time. One partial response time test is run for the sensor and
        associated logic response times. (There should be two trains tested,
        one for low low reactor water level and one for high drywell pressure.)
        The second test is a single HPCI autostart response time test. This
        section uses a simulated signal injection at an appropriate overlap
        point with the low low reactor water level sensor logic.      However,
        there was not an adequate overlap point with the high drywell pressure
        logic train to consider the response time of all its associated relays.
        The response time of the E41-K4 and E41-K5 and E41-K5 relays (high
        drywell pressure initiation relays) was not considered in the total
        high drywell pressure response time test.
        The licensee conducted a Plant Nuclear Safety Committee (PNSC) meeting
        concerning the implications of this problem.       The PNSC concluded
        that: (1) The design response time of the individual relays in
        question as compared to the total response time required by Technical
        Specifications was minimal. The requirement is less than or equal to
        30 seconds. The last HPCI system response time test was 29.64 seconds.
        The licensee had no history of this type relay failing a response time
        test. The design response time of these relays was .08 seconds. Based
        on this information, the HPCI system was not considered inoperable.
        (2) Plant conditions were: Unit 2 power level at approximately 90%,
        'A' loop of Residual Heat Removal (RHR) System under Limiting Condition
        for Operations (LCO), No. 3 Diesel Generator under LCO for maintenance.
        To response test the relay, wires would be lifted and HPCI declared
        inoperable. This would have put the unit outside its LCO action
        statement and into LCO 3.0.3, which requires the reactor shutdown to
        hot standby in 6 hours. The 'A' RHR loop was expected back in service
        that afternoon, and No. 3 Diesel Generator returned Monday, June 24,
        1985.    (3) Plant management decided to test HPCI once a special

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          procedure (SP-85-071) was written and No. 3 Diesel Generator was
          returned to service.
          Technical Specification 6.8.1.c requires that adequate procedures be
          implemented covering surveillance and test activities of safety related
          equipment. Technical Specification 4.3.3.3. requires an ECCS response
          time test to be conducted every 18 months. Contrary to this require-
          ment, the licensee did not establish an adequate procedure for
          Technical Specification 4.3.3.3., in that the testing procedure,
          PT-45.3.4., HPCI Initiation Response Time Test, did not test all the
          relays in the high drywell pressure initiation logic. This violation
          of NRC requirements was identified by the licensee and meets the
          requirements of 10 CFR Part 20, Appendix C     Section V. A.  A Notice of
          Violation will not be issued.
       b. Refuel Hoist Slack Cable Interlock
          On June 8, 1985, defueling of the Unit I core was halted following
          continued problems with the main hoist refuel grapple. The problems
          resulted from slack cable interlock actuations during normal refuel
          grapple operations. While investigating the interlock malfunction and
          conducting corrective maintenance, PT 18.1, Refueling Position Inter-
          lock Check, was found to be inadequate.
          Technical Specification Surveillance Requirement 4.9.6.d states that
          each crane or hoist used for the movement of fuel be demonstrated
          operable by insuring operation of the slack cable cutoff when the load
          was less than 50 plus or minus 25 pounds for the mast fuel gripper.
          Technical Specification 6.8.1.a. requires the licensee to establish
          implementing procedures recommended in Appendix 'A' of Regulatory Guide
          1.33, November 1972. Item H.2 of the guide specifies that procedures
          are required for each surveillance test, inspection and calibration
          listed in the Tcchnical Specification.
          Contrary to the above, PT-18.1 did not demonstrate that the slack cable
          cutoff occurred within the required tolerance. Step 7.3.5 of PT-18.1
          only functionally checked the operation of the slack cable cutoff but
          did not verify the setpoint of the interlock.          This inadequacy
          constitutes a violation 325,324/85-16-01; Inadequate Surveillance Test
          Procedure for the Refueling Hoist Slack Cable Interlock. The licensee
          has revised the procedure to include a setpoint verification and
          completed the test satisfactorily prior to resuming defuel operations.
          This procedure deficiency was also identified in 1983 during a
          Technical Specification review by the Onsite Nuclear Safety Group, but
          an unsatisfactory resolution of the issue left the procedure as is.
          The failure to resolve the issue properly appears to have resulted from
          a lack of understanding of the Technical Specification and the fuel
          grapple operation. Onsite Nuclear Safety is currently reviewing
          additional comments generated during the 1983 review to identify
          similar problems.

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           c.   Diesel Generator Rocker Arm Assembly Nuts
                During observation of PT-12.3.1, for Emergency Diesel Generator No. 4,
                the inspector observed the some of the nuts which attach the rocker arm
                assembly to the cylinder head appeared to be cracked.       Inspection by
                the licensee revealed 21 nuts which were suspect and were replaced.
                During a subsequent performance of PT-12.3.1, for Diesel Generator
                No. 3, the licensee replaced 30 similar nuts. The licensee has sent
                 several nuts to the Harris Energy Center for metallurgical examination.
                Preliminary results indicate that, if the nut does not fail during
                 installation, it will not fail during diesel generator operation. The
                 inspector will review the final report when issued. The licensee plans
                 to inspect diesel generators 1 and 2 during July and replace nuts as
                necessary.
        6. Operational Safety Verification (71707)
           The inspectors verified conformance with regulatory requirements by direct
           observations of activities, facility toars, discussions with personnel,
           review of records and independent verification of safety system status.
           The inspectors verified that control room manning requirements of 10 CFR
           50.54 and the Technical Specifications were met. Control room, shift
           supervisor, clearance and jumper / bypass logs were reviewed to obtain
           information concerning operating trends and out of service safety systems to
           ensure that there were no conflicts with Technical Specifications Limiting
           Conditions for Operations. Direct observations were conducted of control
           room panels, instrumentation and recorder traces important to safety to
           verify operability and that parameters were within Technical Specification
           limits. The inspectors observed shif t turnovers to verify that continuity
           of system status was maintained.       The inspectors verified the status of
           selected control room annunciators.
           Operability of a selected ESF train was verified by insuring that: each
           accessible valve in the flow path was in its correct position; each power
           supply and breaker, including control room fuses, were aligned for
           components that must activate upon initiation signal; removal of power from
           those ESF motor-operated valves, so identified by Technical Specifications,
           was completed; there was no leakage of major components; there was a proper
           lubrication and cooling waster available; and a condition did not exist
           which might prevent fulfillment of the system's functional requirements.
           Instrumentation essential to system actuation or performance was verified
           operable by observing on-scale indication and proper instrument valve
           lineup, if accessible.
           The inspectors verified that the licensee's health physics procedures were
           followed. This included a review of area surveys, radiation work permits,
           posting, and instrument calibration.
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      The inspectors verified that:    the security organization was properly manned
      and that security personnel were capable of performing their assigned
      functions; persons and packages were checked prior to entry into the
      protected area (PA); vehicles were properly authorized, searched and
      escorted within the PA; persons within the PA displayed photo identification
      badges; personnel in vital areas were authorized; effective compensatory
      measures were employed when required; and security's response to threats or
      alarms was adequate.
      The inspectors also observed plant housekeeping controls, verified position
      of certain containment isolation valves, checked clearances, and verified
      the operability of onsite and offsite emergency power sources.
      No violations or deviations were identified.
   7. Onsite Review Committee (40700)
      The inspectors attended selected Plant Nuclear Safety Committee meetings
      conducted during the period. The inspectors verified that the meetings were
      conducted in accordance with Technical Specification requirements regarding
      quorum membership, review process, frequency and personnel qualifications.
      Meeting minutes were reviewed to confirm that decisions / recommendations were
      reflected in the minutes and followup of corrective actins was completed.
      No violations or deviations were identified.
   8. Onsite Review of Licensee Event Reports (92700)
      The listed Licensee Event Report (LER) was reviewed to verify that the
      information provided met NRC reporting requirements. The verification
      included adequacy of event description and corrective action taken or
      planned, existence of potential generic problems and the relative safety
      significance of the event. Onsite inspections were performed and it was
      concluded that necessary corrective actions had been taken in accordance
      with existing requirements, licensee conditions and commitments.         The
      following report is considered closed:
           (Closed) LER 2-83-35; Reactor Water Cleanup differential flow indicator
           was Indicating high because instrument had a low output signal.
      No violations or deviations were identified.
   9. Followup on Inspector Identified and Unresolved Items (92701)
      (0 pen) IFI 325,324/84-35-02; Post-Trip Review.      The inspectors reviewed
      01-22, Plant Incident and Post-Trip Investigation, Rev.10, to ensure that
      an adequate post-trip review program was established. 01-22 was also
      reviewed as part of the Generic Letter 83-28 inspection (85-14). No trips
      have occurred since the latest revision to 01-22. This item will remain
      open pending implementation review of 01-22.
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          (Closed) IFI 324/82-08-07 and 325/32-08-07, Post Potentially Contaminated
          Areas Until Survey Shows Otherwise. The event was reviewed with the
          appropriate personnel at the time of the event. The inspector verified that
          step 8.6.4 of the current revision (No. 4) to procedure E&RC, Posting of
          Areas / Materials, instructs personnel as follows: " . . area that has the
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          potential to be contaminated from occurrences (... leak from a...potentially
          contaminated system...) should be posted as a Contaminated Area until a
          survey. . .can be performed. . .". This procedure adequately addresses the
          inspector's concerns.
          No violations or deviations were identified.
     10. Design, Design Changes and Modifications (37700)
          The inspectors reviewed selected modifications to verify that: activities
          were conducted in accordance with appropriate specifications and drawings;
          appropriate administrative controls were implemented; and acceptance testing
          was appropriate.     The inspectors reviewed portions of the following
          modifications:
                Plant Modification 82-219Q    "B" Loop RHR Service Water.
                Plant Modification 82-287H,0 - Reactor Instrument Penetration Valve
                  Replacement.
                MI-16-35A,C - HFA Relay Reconfiguration and Replacement.
                Plant Modification 1-82-271, Level Transmitter LT-N026A&B
                  Replacement.
          While reviewing a proposed Plant Modification 84-058, the licensee
          discovered a wiring error for the RHR "20" Pump loss of Suction Trip in the
          remote shutdown mode.     The specific error involved u HFA relay in the
          2-E11-F009 valve logic.
          This error would have prevented the operation of the 20 RHR pump in the
          shutdown cooling node from the remote shutdown panel. No other modes of
          operation were affected.     The problem was corrected immediately under a
          trouble ticket.
          The licensee conducted additional system logic drawing review and field
          investigation of the remote shutdown systems. During this review, numerous
          drawing errors, logic errors and incorrectly wired HFA relays were
          discovered. Many of the drawing and logic errors had been corrected in the
          field but the as-built condition was not reflected on the prints. Except
          for the 2-E11-F009 valve logic error, no other problem identified to date
          affected the operability of any equipment in any mode of operation.
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         The problems appear to have been caused by an installation deficiency
         associated with the contact numbering convention for the HFA relays,

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         depending on whether the relay was flush or recessed mounted. The plant
         modification installing the remote shutdown system in 1977 did not
         adequately verify that:     (1) the wiring was in accordance with the drawings,

l (2) the as-built condition was correct or, (3) the acceptance testing was l adequate, i Since this installation, the Plant Modification Procedure (ENP-03) has been l revised and in the inspector's judgement would preclude this situation from l occurring again.

         The licensee's engineering staff has proposed the following corrective
         actions:
         a.    Review logic and drawings associated with the remote shutdown circuitry
               for wiring and drawing discrepancies.
         b.    Complete as-built verification of remote shutdown circuitry and
               identify discrepancies between the as-built and plant drawings.
         c.    Initiate and perform required repairs to correct errors through the use
               of plant modifications or work requests.
         d.    Perform acceptance testing through the use of special procedures that
               will test the remote shutdown system in all modes of operation.
         e.    C1a' rify drawing orientation of HFA relays to distinguish between the
               two relay configurations.

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         Prior to this event, the licensee had already undertaken a program to test
         the dif ferent modes of remote shutdown (1984 - 1985). To'date, only the
         Reactor Core Isolation Cooling System had been satisfactorily tested. Plant
         operating conditions prevented further testing.
         Inspector Followup Item (IFI) 325,324/85-16-02; Remote Shutdown Panel Wiring
         Deficiencies, will track the licensees' actions and progress in this area.
         No violations or deviations were identified.
     11. Refueling Activities (60710)
         During the licensee's defueling operations, the inspectors verified that
         surveillance testing required by Technical Specifications was current and
         that the licensce's fuel handing procedures were implemented. The following
         items were verified:
         a.    Selected fuel bundle movements and storage locations.

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         b.    Core monitoring during defuel operations was in accordance with

l Technical Specifications. l l

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i 10 l l c. Vessel water level was maintained in accordance with Technical l

               Specifications.

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           d.  Reactor mode switch position was as required by Technical Specifica-
               tion.
           e.  Continuous comunications were maintained between the refueling

! platform and the Control Room and the Control Room operators were

               cognizant of the applicable procedure steps,
           f.  Health-Physics personnel maintained constant coverage of all fuel
               moving activities, ensuring area dose rates, contamination levels and
               airborne samples were within required tolerances.
           No violations or deviations were identified.
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