ML20128F880

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Forwards Evaluation Phase Interim Status Rept Re Appraisal of Plant & Sys Operating Procedures in Response to 840618 NRC Order.Evaluation Phase of Appraisal Plan Completed on 850430
ML20128F880
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 05/01/1985
From: Bishop D, Duvall F
OPERATIONS ANALYSIS CORP.
To: Murley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
EA-84-039, EA-84-39, OAC-85-062, OAC-85-62, NUDOCS 8505290751
Download: ML20128F880 (7)


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May 1, 1985

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  • l. 4/ws=Ms *f Dr. Thomas E. Murley, Administrator d'# 4 /* W Region I, Office of Inspection and Enforcement V/.18/8f U.S. Nuclear Regulatory Commission gp fy / uA og,a'$

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Subject:

Appraisal of Plant and System Operating Procedures

Dear Dr. Murley:

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By the NRC Order dated June 18, 1984, the Philadelphia Electric (p g Jwnc+

Company was directed to submit a plan for conducting an appraisal of -

the licensee's plant and system operating procedures. The Appraisal C*N###

Plan was submitted as Attachment B to the Philadelphia Electric CompanyN#

letter dated August 16, 1984. The Appraisal Plan was approved by the Nuclear Regulatory Commission in early September 1984. 7' MJts*

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In accordance with Mr. S.L. Daltroff's letter of September 7, 1984 Ap.4

_it was acreed between the Philadelphia Electric Company and the 4p a Nuclear Regulatory Commission that at the completion of the Evaluation p../ /F4 Phase of the subject appraisal an interim report unnld_be forwarded to y f

% Nuclear Regulatory Commission._The Evaluation Phase was completed Cn April 30, 1985. The Evaluation Phase Interim Status Report is ottached.

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Simultaneous with this transmission, a copy of this letter and its ly Gnclosure is forwarded to Mr. George A. Hunger, Nuclear Safety Section of the Philadelphia Electric Company. Mr. Hunger was designated as

! the liaison between the Philadelphia Electric Company and the project l Appraisal Team. Mr. Hunger and his staff assisted the Appraisal Team l by arranging for documents to be available for the examination of plant and system operating procedures during the Evaluation Phase.

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, This transmittal completes the Evaluation Phase of the Appraisal l Plan. ,

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Enclosure:

Evaluation Phase Interim Report I l

cc: Mr. George A. Hunger {' 3 ll

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May 1, 1985 OAC-85-062 Dr. Thomas E. Murley, Administrator Region I, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 Docket Nos. 50-277 50-278 EA No. 84-39

Subject:

Appraisal of Plant and System Operating Procedures

Dear Dr. Murley:

By the NRC Order dated June 18, 1984, the Philadelphia Electric Company was directed to submit a plan for conducting an appraisal of the licensee's plant and system operating procedures. 'The Appraisal Plan was submitted as Attachment B to the Philadelphia Electric Company letter dated August 16, 1984. The Appraisal Plan was approved by the Nuclear Regulatory Commission in early September 1984.

In accordance with Mr. S.L. Daltroff's letter of September 7, 1984 it was agreed between the Philadelphia Electric Company and the Nuclear Regulatory Commission that at the completion of the Evaluation Phase of the subject appraisal an interim report would be forwarded to the Nuclear Regulatory Commission. The Evaluation Phase was completed on April 30, 1985. The Evaluation Phase Interim Status Report is attached.

Simultaneous with this transmission, a copy of this letter and its enclosure is forwarded to Mr. George A. Hunger, Nuclear Safety Section of the Philadelphia Electric Company. Mr. Hunger was designated as I the liaison between the Philadelphia Electric Company and the project Appraisal Team. Mr. Hunger and his staff assisted the Appraisal Team by arranging for documents to be available for the examination of plant and system operating procedures duri'N the Evaluation Phase.

This transmittal completes the Enr3 un on Phase of the Appraisal Plan.

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F.C.'Duvall, Team Membaz

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Enclosure:

Evaluation Phase Interim Report cc: Mr. George A. Hunger u

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EVALUATION PHASE INTERIM STATUS REPORT INTRODUCTION This Interim Report documents the completion of the Evaluation Phase of the " Appraisal Plan'for the Review of Peach Bottom Atomic Power Station's Plant and System Operating Procedures" as sub-mitted by the Philadelphia Electric Company on August 15, 1984.

The Appraisal Plan was in response to your Order Modifying Licence Effective Immediately, dated June 18, 1984. As agreed between Mr. Richard Starostecki of the Nuclear Regulatory Commisssion and Mr. Shields L. Daltroff, Vice President, Electric Production, Philadelphia Electric Company, an Interim Status Report is to be submitted at.the completion of the Evaluation Phase. The projected completion date of the Evaluation Phase was to be May 4, 1985.

The Evaluation Phase was completed on April'30,'1985.-

The Screening Phase of the Appraisal was completed on February 8, 1985 and an Interim Report was submitted by Operations Analysis Corporation letter OAC-85-018, dated February 8, 1985. , ,

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., e METHODOLOGY The work performed during the Screening Phase consisted of examining the Peach Bottom Technical Specification and FSAR to identify items which established the actions, setpoints, limits, cautions, sequences, and parameters necessary for safe operation.

Each such item was labelled a Procedure Presentation Item (PPI) .

The Screening Phase efforts yielded a total of one thousand four 4

hundred and seventy (1,470) Procedure Presentation Items. The Procedure Presentation Items comprise the Requirements List (formerly called the Requirement Screening List) database.

The Evaluation Phase consisted of searching the Peach Bottom plant and system operating procedures to determine whether the Procedure Presentation Items were actually " included in" appropriate procedures. Each Procedure Presentation Item located in the plant and system operating procedures was entered on the Requirements List. If a Procedure Presentation Item was located in multiple station procedures, all of the procedures were entered into the database.

During the course of the Evaluation Phase one deviation was found.

(A deviation is an instance in which a Procedure Presentation Item is incorrectly or inproperly incorporated into a procedure.) The deviation involved the torus water level lower limit. The Technical Specification value is 14.6 feet. In eight (8) procedure usages the correct value was used. In one (1) procedure (Procedure COL GP-2A, Revision 5, " Reactor Startup Order") an incorrect value of 14.5 feet was given.

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.. 5 METHODOLOGY (continued)

Procedure COL GP-2A was promptly changed, then reviewed.

Approval of the change was recommended by the Peach Bottom Plant Operating Review Committee within one (1) hour of the Operations Analysis Corporation notification of the deviation. The deviation was subsequently found in two (2) other procedures. These procedures were COL GP-2A SINGLE LOOP, Revision 0, " Reactor Startup Order - Single Loop Operation" and ST 10.4, Revision 13,

" Relief Valve Manual Actuation". These procedures were immediately corrected in the same manner. Note: The Technical Specification 1ower limit on torus volume is expressed in terms of cubic feet rather than water level in feet. To ensure accuracy, a secondary calculation of torus volume versus torus water level was conducted by Operations Analysis Corporation. This analysis verified the correspondence of the torus low volume limit (in cubic feet) with the low level limit (in feet of water) as now correctly expressed in all of the Peach Bottom procedures.

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7 9-REQUIREMENTS LLST DATABASE ADJUSTMENTS ,

. i The Requirements List continued to be adjusted by Operations l

Analysis Corporation personnel during the Evaluation Phase. The following adjustments occurred: Three (3) Procedure Presentation Items-were eliminated. Twenty-seven (27) Procedure Presentation Items were deleted when scrutiny confirmed that they did not meet the criteria of the Appraisal. Thirty-five (35) of the Procedure

Presentation Items added during the Screening Phase as the result of Technical Specification Revision 102/104 were deleted from l consideration in this appraisal. It was determined during the Evaluation Phase that these Procedure Presentation items did not l l

meet the Appraisal Plan Criteria and are not related to plant or System Operating Procedures.

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l Of the one thousand four hundred and seventy (1,470) Procedure Presentation Items identified during the Screening Phase, sixty-five (65) were eliminated from the database during the Evaluation Phase. The Evaluation Phase concluded with one thousand four hundred and five (1,405) Procedure Presentation Items. During the Evaluation Phase eighty-nine (89%) percent, or one thousand two hundred and forty-five (1,245) Procedure Presentation Items were confirmed to be correctly " included in" appropriate plant and system operating procedures.

Due to the large number of Procedure Presentation Items and voluminous number of procedures identified in the Appraisal Plan, the Evaluation Phase is regarded as a " rough cut" for confirming the location of Procedure Presentation Items. The remaining Procedure Presentation Items are addressed during the Detaile'd Review Phase.

The Detailed Review Phase is the thorough search of plant and i system operating procedures to determine if the remaining one hundred and sixty (160) Procedure Presentation Items are

" included in" the procedures. The Detailed Review Phase is currently in progress. The results of the Detailed Review Phase j will be provided in the Final Report that is to be submitted to l

the Nuclear Regulatory Commission and the Philadelphia Electric Company by Operations Analysis Corporation in September 1985.

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