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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
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ACCELERATED DOCUMENT DISTRIBUTION SYSTEM REGULA%I INFORMATION DISTRIBUTIOIQISTEM (RIDS)
ACCESSION NBR:9307220073 DOC.DATE: 93/07/13 NOTARIZED: NO DOCKET ¹ FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 AUTH. NAME AUTHOR AFFILIATION TOMONTO,R.J. Florida Power & Light Co.
PLUNKETT,T.F. Florida Power & Light Co. R RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 93-001-01:on 930115,Westinghouse notified util that wet annular burnable absorber assemblies not mf g per design specs. Caused by failure to translate design requirement to drawing absorber design modified.W/930713 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2-2 PD 1 1 RAGHAVAN,L 1 1 .D INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB NRR/DRIL/RPEB l.
1 1
1 NRR/DRCH/HOLB NRR/DRSS/PRPB 1
2 1
2 NRR/DSSA/SPLB EG= 02 1,
1 1
1 NRR/DSSA/SRXB RES/DSIR/EIB 1
1 1
RGN2 FILE 01 1 1 EXTERNAL: EG6G BRYCE,J.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
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.JUL 18 1833 FPL L-93-169 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Gentlemen:
Re: Turkey Point Units '3 and 4 Docket No. 50-250 and 50-251 Reportable Event: 93-001-01 Date of event: January 15, 1993 Axiall Mis ositioned Wet Annular Burnable Absorber WABA Rods The attached Supplement 1 to Licensee Event, Report 250/93-001-00 is being provided, pursuant to the requirements of 10 CFR 50.73 to present the results of further analysis of this event.
Very truly yours, T. F. Plunkett Vice President Turkey Point Nuclear TFP/RJT/rt Attachment cc: S. D. Ebneter, Regional Administrator, Region II, USNRC R. C. Butcher, Senior Resident Inspector, USNRC, Turkey Point t 90':r.
9307220073 930715 PDR ADOCK 05000250 S PDR an FPL Group company
LICENSEE EVENT REPORT (LER)
DOCKET NUMBER (2) PAGE (3)
FACILITY NAME (1)
Turkey Point Unit 3 05000250 . 1 F 6 TITLE (4) Axially Mispositioned Wet Annular Burnable Absorber (WABA) Rods EVENT DATE (5) LER NUMBER(6) RPT DATE (1) OTllER FACILITIES INVOLVED (8)
HON DAY YR YR SEQ 9 Rl HON DAY YR FACILITY NAMES DOCKET 9 (S) 1 15 93 93 001 01 1 13 93 TURKEY POINT UNIT 4 05000251 OPERATING MODE (9) OTHER S ecif in Abstract below and in text Voluntar PONER LEVEL 10 100 LICENSEE CONTACT FOR THIS LER 12 R. J. Tomonto Licensin En ineer TELEPHONE NUMBER 305-246-7327 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER NPRDS2 CAUSF. SYSTEM MANUFACTURER, NPRDS2 SUPPLEMENTAL REPORT EXPECTED 14 NO YES 0 EXPECTED DAY YEAR (f ee c )etc EXPECTED SUBMISSION DATE TK~~
XKRTXKTON ABSTRACT (1 6 On January 14, 1993, with Turkey Point Units 3 and 4 in Mode 1 (POWER OPERATION) at 100% power, Florida Power and Light (FPL) was notified by Westinghouse Electric Corporation (nuclear fuel supplier) that the wet annular burnable absorber (WABA) assemblies were not manufactured according to the design specification. Both units were operating in Cycle 13.
Specifically, beginning with Unit 3 Cycle 12 reload, FPL introduced a new fuel assembly design feature involving debris resistant fuel rods. The debris resistant design involved increasing the length of the solid fuel zod end cap and repositioning the active fuel height up 1.368 inches from the bottom of the fuel rod. The reload design for Unit 3 Cycle 13 and Unit 4 Cycle 13 required the absorber section of the WABAs be repositioned on center to match the corresponding repositioned active fuel height. During the startup of Turkey Point Unit 3 Cycle 13, FPL measured a higher local peaking factor (Fq) and a more top-peaked beginning of cycle axial power distribution than predicted by core models. As a result of further investigations, Westinghouse determined that the absorber section of the WABA had not been manufactured in accordance with design specification for the fuel reload.
At no point was either Unit 3 or Unit 4 operating in a condition outside of the design bases of the plants.
This LER is submitted as VOLUNTARY.
Lxczzszzvzzx zzzozm (Lzz) mzxm >zxxzvzzxoz FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 93-001-01 02 OF 06 I. DESCRIPTION OF THE EVENT The following chronology of events was developed.
12/29/92 Unit 3 was in Mode 1 at 100% Power (POWER OPERATION) and Unit 4 was in Mode 1 at 100% Power Florida Power and Light (FPL) reviewed the Unit 3 flux map at 100% power (following the initial return to power after a refueling outage), equilibrium xenon, steady-state conditions and found an increase in local peaking factor (Fq), and a more top-peaked beginning of cycle (BOC) axial power distribution than predicted by core models.
12/30/92 FPL reviewed the INCORE-3D code and the trace alignment through procedure. FPL investigated the possibility that the absorber 1/13/93 section of the wet annular burnable absorber (WABA) rods (EIIS-AC) (IEEE-ABS) was not centered with the fuel assembly active .
fuel height.
1/14/93 Westinghouse confirmed that the WABA rods were not manufactured in accordance with design requirements. Westinghouse's calculations showed that the WABAs rods were offset -1.368" from the center of the active fuel.
1/15/'93 Based on the preliminary results obtained from FPL and Westinghouse core models, and engineering judgement, .it was determined that current operation for both units was acceptable.
Westinghouse was 'directed to confirm this conclusion based on performing the Final Acceptance Criteria (FAC) analysis using as-built parameters. A satisfactory interim operability assessment was completed.
1/17/93 Westinghouse completed the FAC analysis using BOC operation data (zod position and power versus time). Westinghouse concluded from the FAC analysis that all operation for both units was bounded by the design basis for the entire fuel cycle.
FPL introduced a debris resistant fuel assembly (DRFA) (EIIS AC) design beginning in Unit 3 Cycle 12 and continuing in Unit 4 Cycle 13 and Unit 3 Cycle 13 reloads. The DRFA design incorporates the following design features compared to the standard Westinghouse optimized fuel assembly (OFA) design:
~ solid bottom fuel rod end plug was increased in length 1.381 inches, by'pproximately total fuel stack height remained unchanged (with the exception of the positioning within the fuel rod), II fuel assembly spacer grids were repositioned, and guide tube dashpot was shortened and guide tube flow hole locations were changed, to accommodate the repositioning of the spacer grids.
LICENSEETENT REPORT (LER) TEXT NTINUATION FACILITY NAME 'OCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 93-001-01 03 OF 06 The Westinghouse DRFA design'is unique to Turkey Point and no other licensee using Westinghouse fuel has incorporated the same fuel assembly design.
Other PWR fuel suppliers utilize this same design. ~
I
.In Unit 3 Cycle 12 a study of the use of offset WABA's concluded that the effects of this offset was not significant. The presence of the offset WABA rods were not discernable during the Unit 3 Cycle 12 startup, since the number of WABA rods (96) did not significantly alter the expected per fozmance of the core.
The Unit 4 Cycle 13 reload included the first Unit 4 batch of fuel with debris resistant fuel. The reload design included 368 WABA rods, distributed in 36 fuel assemblies. The largest number of WABA rods in an individual assembly was 20 rods. The location of the WABA assemblies within core was evenly distributed across the core and exposed to an average 'he power condition. A discrepancy in peaking factors was not observed in the Unit 4 Cycle 13 fluxmaps, since the number of WABA rods and their effect on axial flux shape did not significantly alter the expected performance "of the core. The results of Westinghouse's FAC reanalysis concluded that the core limits were maintained (Fq) during the cycle with the offset WABAs and the offset WABAs did not compromise plant safety.
The Unit 3 Cycle 13 reload represented the second fuel region (in Unit 3) with debris resistant fuel. The reload design included 512 WABA rods,
'istributed in'8 fuel assemblies. The largest number of WABA rods in an individual assembly was 20 rods. The location of the WABA assemblies within
- the core was centered around the middle of the core, corresponding to the highest power density in the core. As highlighted above, FPL discovered, during the initial fluxmap at 100% power steady state conditions, a discrepancy between the predicted and measured total peaking factor (Fq) .
Subsequent investigation of the deviation led to the conclusion that the WABA rods were incorrectly positioned by -1.368 inches relative to the active fuel stack. A safety evaluation was performed to evaluate the acceptability of operation of both units for the remainder of these cycles (Unit 3 Cycle 13 and Unit 4 Cycle 13).
ZZ. CAUSE OF THE EVENT The root cause of this event was that Westinghouse failed to translate a specific design requirement for centering the WABAs to the fabrication drawing.
The following factors contributed to the event:
- 1. FPL correctly specified 0.0 inch WABA offset in the reload specification for Unit 3 Cycle 13 and Unit 4 Cycle 13 reload.
However, FPL did not highlight this dimension as a change to Westinghouse.
- 2. Westinghouse performed an evaluation of the Unit 3 Cycle 12 reload with offset WABAs and concluded that the offset was not significant.
This evaluation was later misinterpreted as a general design guideline.
- 3. The Westinghouse design review process failed to address the location of the WABAs as a design criterion.
LICENSEEVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 93-001-01 04 oF 06 III. ANALYSIS OF THE EVENT A. Turke Point Unit 4 C cle 13 0 eration Turkey Point Unit 4 Cycle 13 reload design was evaluated using"existing core design models with NRC approved methodology. These models were revised to account for the WABA offset and us'ed to verify that the full cycle of operation was bounded by the existing Reload Safety Evaluation. This verification involved evaluating the impact of the WABA offset on the Cycle 13 Reload Safety Analysis Checklist (RSAC) parameters and on the axial power distribution analysis to determine the impact on Departure from Nucleate Boiling (DNB) and Fq.
The RSAC parameters represent a comparison of the nuclear design inputs to the safety analysis input. No accidents were required to be re-evaluated the design inputs are bounded by the safety analysis inputs. The impact of if the WABA offset'on each of the Cycle 13 RSAC parameters was analyzed or assessed for its impact on the current RSAC. The nuclear design. inputs for the WABA offset case were bounded by the current RSAC.
Axial power shapes were analyzed using the NRC approved Final Acceptance Criteria (FAC) methodology. This analysis was re-performed for the entire fuel cycle. For a variety of plant operational maneuvers, this analysis generates thousands of power shapes which represent a family of adverse xenon and power distributions which are possible during Condition I and Condition II events. The FAC re-analysis verified that Fq limits remained below the Technical Specification limits during all Mode 1 operation provided that axial flux distribution (AFD) and rod insertion limits are maintained within the limits allowed by the Technical Specifications.
In summary, all statements and conclusions presented in the original Reload Safety Evaluation (RSE) remain valid for the entire operating cycle. The Unit 4 Cycle 13 core design with offset WABAs meets all safety parameter limits, thereby ensuring that all pertinent design and licensing basis acceptance criteria are met.
B. Turke Point Unit 3 C cle 13 0 eration Similar to Unit 4, the Unit 3 Cycle 13 reload was evaluated using core models which were revised to account for the offset WABA. The RSAC parameter evaluation and FAC analysis were performed from 1000 Megawatt-days/Metric-ton Uranium (MWD/MTU) to the End of Cycle (EOC) . The current burnup exceeds 1000 MWD/MTU. The nuclear design inputs for the WABA offset case were bounded by the current RSAC.
,To ensure that Technical Specification compliance had been maintained for Unit 3 Cycle 13 from BOC to 1000 MWD/MTU, past operation data (i.e., actual power history and rod movement) was reviewed and modelled using an approved three-dimensional nuclear code. The analysis demonstrated that the Fq Technical Specification limit was not violated during actual operation and the plant was always within the design basis.
Within the conditions of the Technical Specification, the potential did exist that Unit 3 could have operated outside the design basis; however, at no point did either Turkey Point Units 3 or 4 operate outside their design bases.
x,xczzzzz+vzm zzzozx (zzz) mzzx zznmrzmxoz FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 93-001-01 05 OF 06 C. Re ortabilit Determination Reportability was evaluated under 10 CFR 50.73 (a)'(2). The event of the mispositioned WABA was originally reported under 10 CFR 50.73 (a) (2) (ii) (A) .
The details that follow will address the basis, of the determination of a VOLUNTARY LER.
10 CFR 50.73 (a) (2)(ii)(A) states: Any event or condition that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded, or that resulted in the nuclear power plant being in an unanalyzed condition that significantly compromised plant safety.
For, both Unit 3 Cycle 13 and Unit 4 Cycle 13, the mispositioned WABA rods placed the units in an unanalyzed condit'ion. Both Westinghouse and FPL recognize the fact that the nuclear design analysis and conclusions reached in the reload safety evaluations (RSE) for these cycles were based upon the burnable absorber section of the WABA rods being centered at the midplane of the active fuel. As a result, a change from this assumption, which in itself is less conservative, has placed this event in an unanalyzed condition.
The significance of this unanalyzed condition is evaluated by using the criteria that an unanalyzed condition that significantly compromises plant safety exists if '(1) the condition potentially affecting a component, system, or structure is of more than minor safety significance; and (2) the condition potentially could (a) increase the probability of occurrence or the consequences of an accident or malfunction of equipment. 'ngineering judgment and experience may be used when evaluating the condition for reportability under this criteria.
FPL concluded that the mispositioned WABA rods were of minor safety significance for Unit 3 Cycle 13 (BOC to 1000 MWD/MTU), based on the following information:
The results from the FAC analysis performed by Westinghouse concluded that Fq*K(z) could potentially have been violated by up to approximately 11% based on the WABA offset at approximately 10.6'f the active core height (maximum Fq of 2.425 at 10.6'), if the unit had operated in 'a load-follow mode with the worst combination of axial power shape and rod position.
Based on an Fq of 2.425 and the Westinghouse Power Shapes Sensitivity Methodology (PSSM) for Loss of Coolant Accidents (LOCA), the Peak Clad Temperature (PCT) would have increased approximately 61'F from the current analysis. By FPL letter L-92-338, dated December 18, 1992, FPL submitted to the NRC a summary of the 'current analysis of record for Large Break LOCA of 2129'F. Therefore the PCT would have been .
approximately 2190'F (for this extreme case), which. is less than the 10 CFR 50.46 (b)(1) criteria of 2200'F.
The axial power shapes resulting from the mispositioned WABA for Unit 3 Cycle 13 from BOC to 1000 MWD/MTU are more limiting than those analyzed in the FAC analysis supporting the original reload safety evaluation. Westinghouse performed specific neutronic and thermal hydraulic calculations which confirm 'that the DNBR limit would not have been violated during the operation of Turkey Point Unit 3 Cycle 13, considering all possible power shapes that have occurred, 'or may occur, due to the mispositioned WABAs, throughout the cycle using the
I, r
4 LICENSEEVENT REPORT (LER) TEXT QNTINVATION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 3 05000250 93-001-01 06 OF 06 Constant Axial Offset Control (CAOC) operating strategy.
Additionally, the non-LOCA analyses have been reanaly'zed using the Revised Thermal Design Procedure (RTDP) which results in a DNBR- margin of 19. 6% for the optimized fuel assembly design. This additional margin can also accommodate any reduction in the DNBR due to the mispositioned WABAs. In the reanalyses of the non-LOCA events using RTDP, an Fq of 2 ' with a 5% flow reduction and FaH of 1.70 were used.
The current Fq and FaH limits are 2.32 and 1.62, respectively.
~
For the Unit 3 Cycle 13 core design with offset WABAs, the analysis using actual plant operating history data and rod movement demonstrated that the Fq Technical Specification limit was not violated .during actual operation at BOC (0 to 1000 MWD/MTU) and the plant was always within the design basis.
For the Unit 4 Cycle 13 core design with offset WABAs, the coze design met all safety parameter limits, thereby are ensuring that all pertinent design and licensing basis acceptance criteria met.
In summary, at no point was either-Unit 3 or Unit 4 operating in a condition outside of the design basis of the plant.
As a result, this LER is submitted as VOLUNTARY.
IV. CORRECTIVE ACTIONS
- 1. 'estinghouse modified the design of the WABAs for Turkey Point Unit 4 Cycle 14 to correctly position the absorber section relative to the active fuel height.
- 2. FPL performed an oversight review to determine Westinghouse fuel design process could if have/should the error in the have been identified by the licensee. This oversight review included Engineering and Quality Assurance (QA) activities.
For each future reload, a Reload Oversight Plan will be prepared that 3.
reflects the physical and neutronic changes to the fuel for that cycle. This effort will be implemented beginning with the Unit 3, Cycle 14 reload.
4 FPL performed a review of the burnable absorber positioning at St.
Lucie Units 1 and 2, to determine its applicability to other FPL
~
nuclear fuel suppliers. No problem was identified.
- 5. FPL revised Nuclear Engineering quality instruction (JPN QI) 3.1.8, "Engineering Package (EP) for Fuel Reloads" to facilitate identification of changes to core components oz core response.
V. ADDITIONAL INFORMATION None'.