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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
[Table view] |
Text
ACCEI.ERAT~ DOCUMENT DIST UTION SYSTEM REGULATE INFORMATION DISTRIBUTIO SYSTEM (RIDS)
ACCESSION NBR:9212290181 DOC.DATE: 92/12/17 NOTARIZED: NO -DOCKET ¹ FAC1L:50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH. NAME AUTHOR AFFILIATION TOMONTO,R.J. 'Florida Power a Light Co.
PLUNKETT,T.F. Florida Power 6 Light Co.
RECIP.NAME -
RECIPIENT AFFILIATION
SUBJECT:
LER 92-009-00.:on 921117,measured prestress force on containment tendon lower than predicted lower limit.Caused D by increased tendon wire steel. relaxation loss at higher tendon temp. Lift-off forces restored.W/921217 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: C7 TITLE: '50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES':NRR RAGHAVAN,L 05000251 A RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2=2 PD 1 1 AULUCK,R 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB8H3 1 1 NRR DST/SPLB8D1 1 1 NRR/DST/SRXB 8E 1 1 4REG~ 02 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL EGSG BRYCE I J ~ H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY i G. A 1 1 NSIC POOREIW ~ 1 1 NUDOCS FULL TXT 1 1 NOTES: 1 1
'S A,
D NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
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FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30
41 P.O. Box 029100, Miami, FL, 33102-9100 DH8 1'I 1992 L-92-344 10 CFR 50.73 10 CFR 50.36 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Re: Turkey Point Unit 4 Docket No. 50-251 Reportable Event: 92-009 Date of Event: November 17, 1992 Containment Tendon Surveillance Measured Prestress Force Lower than Predicted attached Licensee Event Report (LER) 251-92-009 is provided
'he pursuant to the requirements of 10 CFR 50.73 (a)(2) (i) (B) to provide information on the subject event. In accordance with NUREG-1022, Supplement 1, this LER will also satisfy the requirements of Technical Specification 3.6.1.6, submittal of a Special Report. ~
Very truly yours, O',P, i~uD/p.
T. F. Plunkett Vice President Turkey Point Nuclear TFPNRJTNrt Attachment cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant PBI O7.
9212290181 921217 PDR *DOCK 05000251 rent
/f S PDR an FFL Grocp compan~
Cl LICENSEE EVENT REPORT (LER)
DOCKET NVNSXR (I) FACE (l)
'FACILITT NAKC (I)
Turkey Point Unit 4 05000251 OF 9 Containment Tendon Surveillance Measured Prestress Force Lower than Predicted RTT DATE (I) OTKtR FACILITItS INV. ( ~ )
EVENT DATE (5) LER NOMBER (6)
SEO I R( DOCKET ( (S)
MON YR NAME 11 17 92 92 009 00 1 17 92 OTIRATINC )COE (S)
~ xxtx txvtt OO 10 CFR 50.73 a 2 i B and OTHER S ecial Re ort (SPOCI(F lh Ahttthtt Nh)OV Xhd lh tezt) 100 LICENSEE CONTACT FOR THIS LER (12)
Robert J. Tomonto, Licensing Engineer 305-246-7327 CONSLETE ONt LINE FOR LACK'CONFONtNT FAILVRE DtSCRISED IN TKIS Rt)ORT (ll)
SISTTN CAVSE EST ECTTD SVFFLXNENTAL RTFORT EXTTCTSD (I ~ ) SVSNISSION MONTH DAY YEAR DAIt (ll)
((I Fhh, COXD)hth XXSSCTSD SVSNISSION CATt> NO AXSTRACT (1()
On November 17, 1992 at approximately 0917 EST, with Turkey Point Unit 3 in Mode 5 (COLD SHUTDOWN) and Unit 4 in Mode 1 (POWER OPERATION), Unit 4 entered LIMITING CONDITION FOR OPERATION (LCO) 3.6.1.6 a., with Unit 4 containment hoop tendon 35H38 measuring an observed lift-off value less than 90% of the predicted lower limit (PLL) . ACTION a. of Technical Specification 3.6.1.6 required that with one tendon below 90% of the PLL, restore the tendon to the required level of integrity within 15 days, perform an engineering evaluation of the containment and provide a Special Report to the Commission within 30 days. In accordance with SURVEILLANCE REQUIREMENTS 4.6.1.6.1, adjacent tendons were checked for their lift-off force. Tendons 35H39, 35H40, 35H41 and 35H42 measured lift-off values between PLL and 90% of PLL.
Tendons 35H38, 35H39, 35H40, 35H41 and 35H42 were retensioned and on November 19, 1992, at approximately 1715 EST, Unit 4 exited LCO ACTION 3.6.1.6 a.
This event is reportable under 10 CFR 50.73 (a) (2)(i) (B) . Operability of tendon 35H38 is established based upon a revision to the calculated value for the predicted lower limit and minimum required prestress force for the Unit 4 containment. These values were initially calculated assuming a maximum containment design pressure of 59 psig, and were subsequently revised to 55 psigx Technical Specification 5.2.2, DESIGN FEATURES DESIGN PRESSURE AND TEMPERATURE, states that "the containment building is designed and shall be maintained for a maximum .internal pressure of 59 psig". Operability of tendon 35H38 is established based upon the licensing basis provided in the original Turkey Point Safety Evaluation Report which states that 55 psig is an acceptable design pressure. FPL will submit license amendments to revise the Technical Specification design pressure to reflect the licensing basis design pressure.
x
~ I I ZCENSEE OENT REPORT (LER) TEXT (TZNUATZON FACILITY.NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 4 05000251 92-009 02 oF 09 X. DESCRIPTION OF THE EVENT The following sequence of events was derived from the Reactor Operator' log and the equipment out-of-service log.
0910 11/17/92 Unit 3 in Mode 5 (COLD SHUTDOWN) and Unit 4 in Mode 1 (POWER OPERATION) performed'he Unit 4 twentieth year tendon surveillance. Hoop tendon 35H38 measured a low lift-FPL off force of 5.94 kips/wire which is equivalent to 89.6% of the predicted lower limit (PLL). Unit 4 entered LIMITING CONDITION FOR OPERATION 3..6.1.6 a.,
with a 15 day ACTION statement requiring the tendon to be restored to the required level of integrity.
1530 ll/17/92 Hoop tendon 35H39 measured a low lift-off force of 6.09. kips/wire or 91.8% of PLL. Tendon 35H39 declared Out-of-Service.
1640 11/17/92 Hoop tendon 35H40 measured a low lift-off force of 6.12 kips/wire or 92.3% of PLY Tendon 3SH40 declared Out-of-Service.
1115 11/18/92 Hoop tendon 35H41 measured'a low lift-off force of 6.01 kips/wire or 90.6% of PLL. Tendon 35H41 declared Out-of-Service.
1200 11/18/92 Hoop tendon 35H42 measured a low lift-off force of 6.13 kips/wire or 92.5% of PLL. Tendon 35H42 declared Out-of-Service.
1130 11/19'/92 Retensioned tendon 35H42, returned tendon to service 1405 11/19/92 Reten ioned tendon 35H41, returned tendon to service 1715 11/19/92 Retensioned tendons 35H38, 35H39 and 35H40, returned tendons to service. Exited LCO ACTION 3.6.1.6 a.
This event- is reportable under 10 CFR 50.73 (a)(2)(i)(B). Operability of tendon 35H38 is established based upon a revision to the calculated value for the predicted lower limit and minimum required prestress force for the Unit 4 containment. These values were initially calculated assuming a maximum containment design pressure of 59 psig and were subsequently revised to 55 psig, which is 110% of current containment peak internal pressure based on design basis LOCA.
'echnical Specification 5.2.2, DESIGN FEATURES DESIGN PRESSURE AND TEMPERATURE states the following:
"The containment building is designed and. shall be maintained for a maximum internal pressure of 59 psig A maximum containment pressure of 55 psig was assumed in the original Turkey Point Safety Evaluation Report (Ref.,5.10) which stated the following:
0
~
I ICENSEE QENT REPORT (LER) TEXT CONTINUATION FACILITY NAME DOCKET NUMBER .LER NUMBER PAGE NO.
TURKEY POINT UNIT 4- 05000251 92-009-00 03 oF 09 "The applicant has now calculated that the peak accident pressure would be 50 psig. Since our current guidelines for .containment design suggest that the design'ressure should be at least 10%
highez than the calculated peak accident pressure, 55 psig would be an acceptable design pressure".
The methodology for calculating both the predicted lower limit and the minimum required pzestress limit has been transmitted to the NRC by FPL Letters L-92-262, dated September 14, 1992 and L-92-287, dated November 5, 1992.
In order to establish operability of tendon 35H38 the maximum containment pressure in the containment structural analysis assumed a value of 55 psig.
II. CAUSE OF THE EVENT By FPL letter L-92-262, dated September 14, 1992, FPL reached the following conclusion, from the Turkey Point Unit 3 twentieth year tendon surveillance:
Based on the engineering evaluation (FPL letter L-92-262), FPL determined that the tendon wire steel relaxation loss increases with the increase in temperature experienced by the tendon. It was also determined that the measured Unit 3 containment internal temperature during suzveillance averaged 114 'F which results in hoop tendon temperature of approximately 90 'F, which corresponds to higher tendon wire steel relaxation losses than those used in the original design. Therefore, the probable cause for the low lift-off forces measured for the Turkey Point Unit 3 containment tendons was increased tendon wire steel relaxation loss hoop occurring at a higher tendon temperature (approximately 90 'F).
Based on the results of this evaluation, it is estimated that a 12% tendon wire teel relaxation loss rate should be used to predict the undisturbed tendon lift-off forces in future surveillances. It is also concluded that creep loss calculated based on the average sustained concrete compressive stress should be used to more accurately predict the tendon lift-off forces in each group (hoop, vertical and dome) in future surveillances.
FPL believes the root cause of the Unit 4 low lift-off forces to be equivalent to the zoot cause of the low lift-off values observed in Unit 3. Consistent with the Unit 3 containment twentieth year surveillance tendon report, a more detailed engineering evaluation is being prepared to investigate the cause and the extent of low lift-off values in the Unit 4 containment structure post-tensioning system.
This evaluation will also determine the length of time that the Unit 4 Turkey Point post-tensioning system will continue to satisfy the licensing basis requirements.
III. ANALYSIS OF THE EVENT FPL's engineering evaluation provides the following:
The licensing basis for the containment design for the acceptability of the low lift-off condition pressure.'ustification on hoop tendon 35H38 and adjacent tendons.
0 I ICENSEE SENT REPORT (LEE) TEXT (TINURTION FACILITY NAME BOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 4 05000251 92-009-00 04 oF 09 1.0 Licensin Basis For Containment Desi n Pressure Containment tendon surveillance inspections performed .to date for Turkey Point,.Units 3 and 4 have assumed a containment internal pressure o'f 59 psig for calculating the minimum design prestress forces. However, due to the low lift-off forces data obtained for hoop tendon 35H38, FPL has calculated the minimum design lift-prestress force zequi.'red to meet 55 psig. The measured low off forces are then evaluated using the minimum design pzestzess force for 55 psig to determine the acceptability of the containment post-tensioning system.
Back round The containment licensing basis pressure of 55 psig was established during the early stages of plant licensing (circa 1965 1966) and has carried through to current licensing documents. The Preliminary Safety Analysis Report (PSAR) and Updated Final Safety Analysis Report (UFSAR) indicated that a 55 psig reference containment licensing basis pressure was conservatively established for the design basis (29-inch double-ended pipe break) loss-of-coolant accident (LOCA), based on a 49.9 psig calculated peak pressure plus a 10% safety margin. The structural proof test was conducted at 115% design pressure to verify structural integrity. .[Reference PSAR Sections 5.4.1.a and 12.2.3; and Reference UFSAR Revision 4 dated'ugust 12, 1970, Section 5.1.1]
Other LOCA cases, assuming partial safeguards availability, were also considered. These cases did not constitute design basis accident scenarios, but rather provided an indication of potential containment performance requirements beyond-the-licensing-basis for purposes of establishing a conservative design for the containment. These scenarios were considered in response to Atomic Energy Commission (AEC) questions, to address uncertainties in the availability of accumulators. As a result,,
these other cases assumed partial safeguards operation with no core cooling; conditions that are beyond the required postulation of a single active or passive failure [Re'ference PSAR Supplement 2, Questions 1.0 and 3.0, dated 9/2/66]. The value of 55 psig was determined as the licensing basis analysis for partial safeguards availability, by operating on diesel power, and providing core cooling by having 2/3 of the available safety injection water reach the core.
To accommodate these hypothetical, beyond-the-licensing-basis scenarios, the containment structure was originally designed assuming a peak pressure of 59 psig; however, the design basis LOCA calculated peak pressure was 49.9 psig, and "55 psig was considered as nominal structural design pressure, thus allowing a margin of 10% over the calculated peak accident pressure."
[Reference UFSAR Revision 4 dated August 12, 1970, Section 5.1.1]
0 t LICENSEE ~T REPORT (LER) TEXT ClINURTION'ACILXTY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 4 05000251 92-009-00 05 oF 09 Based on the AEC Safety Evaluation Report (SER): 55 psig is the licensing basis containment design pressure; this value is based on a calculated design basis LOCA peak pressure of 49.9 psig plus a safety margin; and the internal pressure of 59 psig was selected based on non-licensing basis LOCA scenarios. This is consistent with the AEC conclusions presented in the plant SER, (Section 5.4 of Reference 5.10) which states:
"Although the building is designed to withstand a pressure of 59 psig, the preopezational structural proof test was performed at about 63 psig rather than at 68 psig (115% of 59 psig) .
The design pressure was established at the construction permit stage based upon an early containment pressure transient analysis which did not take credit for the action of the accumulators in suppressing a secondary pressure peak. The applicant has now calculated that the peak accident pressure would be 50 psig. Since our current guidelines for containment design suggest that the design pressuie should be at least 10's higher than the calculated peak accident pressure, 55 psig would be an acceptable design pressure. On this basis we have accepted the 63 psig proof test (115% of 55 psig)".
The LIMITING CONDITION FOR OPERATION foz structural integrity ensures that the containment will withstand the maximum pressure the event of a LOCA. [Reference 5.2, Bases Section 3/4.6.1.6;
'n and Reference 5.1, Section 5.1.1]
1.1 Licensin Basis Early performance requirements for the containment were added to address the uncertainty in component availability for LOCA scenarios. The licensing basis for containment design pressure is 55 psig based on a calculated design basis LOCA peak pressure of 49.9 psig plus a margin of safety. Because the calculated peak pressure is less than the licensing basis containment design pressure'f 55 psig, as required at the operating license stage, using 55 psig for calculating minimum design prestress forces does not impact the margin of safety.
2.0 En ineerin Evaluation of Hoo Tendon 35H38 Low Lift-Off Condition The Turkey Point Unit 4 containment is a post-tensioned, reinforced concrete structure comprised of a vertical cylinder with a shal'low dome and supported on a conventional reinforced concrete foundation base slab. The vertical cylinder wall is provided with a system of vertical and hoop tendons. Vertical tendons are anchored at the top surface of the ring girder and at the bottom of the base slab. Each hoop tendon is anchored at alternate vertical buttresses nominally 120 degrees in the dome consist of three groups of tendons oriented apart'endons at 120 degrees with respect to each other and are anchored at the vertical face of the dome ring girder.
II 0 LICENSEE ENT REPORT (LER) 'EXT CTINCRTION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE No.
TURKEY POINT UNIT 4 05000251 92-009-00 06 oF 09 The tendon surveillance program for the Turkey Point Nuclear Plant Unit 4 containment structure post-tensioning system has been. performed at one, three and five years after the containment Initial Structural Integrity Test, (ISIT), and every five years thereafter. Three dome, five hoop, and, four vertical tendons were selected for the t'wentieth year tendon surveillance on a random basis, excluding those tendons which were previously inspected for earlier surveillances. The Turkey Point Unit 4 twentieth year tendon surveillance i's performed in accordance with the requirements of References 5.6 and 5.9.
To date, a wire has been zemoved for inspection from dome tendon 1D40, and hoop tendon 42H83. In addition, grease samples have been removed for each surveillance tendon inspected to date. The visual inspection of the tendon wire and sheath filler samples have revealed no abnormal wire corrosion or grease discoloration.
Also, the concrete at the tendon anchorage area adjacent to the bearing plates for all hoop tendons has been inspected. This inspection has revealed that no cracks were found which exceed the acceptance width of 0.01 inches noted in Reference 5.8, Section IWL-3221.3(d).
FPL has calculated that the minimum design prestress force for hoop tendons required to withstand 55 psig containment internal pressure is 5.94 kips/wire at the anchorage (Reference 5.5) .
Considering the 55 psig internal pressure and the minimum required prestress force of 5.94 kips/wire for hoop tendons, this calculation has determined that the conclusions of the original containment analysis will not be adversely affected.
The following are the predicted lower limit (PLL) and the minimum design prestress force at the anchorage for hoop tendons:
e Twentieth Year Predicted Lower Limit 6.63 kips/wire (Reference 5.6)
Minimum Design Prestress Force 5. 94 kips/wire (at anchorage for Hoop Tendons)
(Reference 5.5)
The lift-off forces which are below the predicted lower limit occurred in one of the hoop surveillance tendons (35H38) and its adjacent tendons (35H39, 35H40, 35H41 and 35H42). Due to accessibility problems below tendon 35H38, all adjacent tendon lift-off testing was performed above tendon 35H38. The following summari'zes the results of the lift-off forces on hoop tendon 35H38 and its adjacent tendons:
Oi V
LICENSEE ENT REPORT (LER), TEXT dQTINURTION FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 4 05000251 92-009-00 07 OF '09 Measured Normalized 'Percentage Tendon Lift-Off Force ki s wire of PLL 35H38 5.94 89 ..6%
35H39 6.'09 91.9%
35H40 6.12 92.3%
35H41 6.01 90.6%
35H42 6.13 92.'5%
Average 6. 06 kips/wire 91.4%
As shown, the individual lift-.off force and the average lift-off force for the group is equal to or larger than the minimum design prestzess force (5.94 kips/wire). Therefore, it that the subject tendon group presently provides adequate is concluded prestzess force to maintain the containment integrity. This conclusion is consistent with the guidance provided in Section 7.1.5 of Regulatory Guide 1.35 (Reference 5..7) and Section IWL-3221.1 (a) of ASME Code (Reference 5.8).
A more detailed engineering evaluation is being prepared to investigate the cause and the extent of low lift-off values in the Unit 4 containment structure post-tensioning system. This evaluation will also determine the length of time that the Unit 4 Turkey Point post-tensioning system will continue to satisfy the licensing basis requirements. A report will be submitted to the NRC by January 29, 1993.=
3.0 Desi n Mar ins Available in the Post-Tensionin S stem Turkey Point UFSAR (Reference 5.1), Section 5.1.2 states that any three adjacent tendons in any tendon group can be lost without significantly affecting the strength of the containment structure. This design feature considers the load redistribution ~
capabilities of the containment shell.
4.0 Conclusion The licensing basis containment design pressure is 55 psig as established in the original Turkey Point Safety 'Evaluation Report (Reference 5.10) and is the appropriate basis for containment structural analysis to evaluate the containment post-tensioning system.
Based on the available margins existing in the design of the Turkey Point post-tensioning system and the level of pzestress force available in the subject hoop tendons, it is concluded that the Unit 4 hoop tendon group presently have sufficient prestress force to maintain the containment integrity.
A more detailed engineering evaluation is being prepared to investigate the cause and the extent of low lift-off condition in the Unit 4 containment structure post-tensioning system. This evaluation will also determine the length of time that the Unit 4 Turkey Point post-tensioning system will continue to satisfy the Turkey Point licensing basis requirements. A report will be submitted to the NRC by January 29, 1993.
4i LICENSEEVENT REPORT .(LER) TEXT QNTZNUlLTZON FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 4 05000251 92-009-00 08 oF 09 5.0 References 5..1 Turkey Point Units 3 and 4 Updated Final Safety Analysis Report (UFSAR), Revision 10, dated July 1992, Section 5.0 5.2 Technical Specifications, Amendment 152/147,, Sections 4.6.1.6.1(a) and 3.6.1.6.
5.3 Bechtel Calculation No. C-SJ539-05, "Evaluation of the Fifteenth Year Tendon Surveillance Lift-Off Forces",
Revision 0
=5.4 Non-Conformance Report N-92-0306 5.5 Bechtel Calculation No. C-SJ561-03, "Evaluation. of the Unit 4 Twentieth Year Tendon Surveillance Low Lift-Off Forces",
Revision 0 5.6 Bechtel Technical Requirements Document 21701-561-CP-1, Revision 0, for Unit 4'wentieth Year Tendon Surveillance 5.7 Regulatory Guide 1.35, "In-service Inspection of Ungrouted Tendons in Prestressed Concrete Containment", Revision 3, dated July 1990 5.8 ASME Code, 1989 Edition,Section XI Division 1, Article INL-3000 "Acceptance Standards" 5.9 Turkey Point Plant Procedure O-SMM-51.2, "Containment Tendon Inspection", dated June 26, 1992 5.10 AEC Letter from R. C. DeYoung to Dr. J. Coughlin, Florida Power and Light Company, Safety Evaluation by the Divis'ion of Reactor Licensing, Turkey Point Units 3 and 4, dated March. 16, 1972
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t LICENSEE ENT REPORT (LER) TEXT CTTNUATTON FACILITY NAME DOCKET NUMBER LER NUMBER PAGE NO.
TURKEY POINT UNIT 4 05000251 92-009-00 09 oF 09 ZV. CORRECTIVE ACTZONS 1n accordance with Turkey Point Technical Specifications ACTION 3.6.1 6 (a), the
~ lift-offPlant forces in tendons 35H38, 35H39, restored to their required level 35H40, 35H41 and 35H42 have been of integrity by retensioning each tendon to a level equal to or above the twentieth year predicted lower limit (6.63 'kips/wire).
The following summarizes the new lift-off forces for the subject tendons:
Measured Percenta e of Tendon Avera e Lift-Off ki s Predicted Lower Limit 35H38 622.3 104.3%
35H39 618.7 103.7%
35H40 631.8 105.9%
35H41 614.4 103.0%
35H42 623.2 104.4%
- 2. A more detailed engineering evaluation is being prepared to investigate the cause and the extent of low lift-off values in the Unit 4 containment structure post-tensioning sy'tem. This evaluation will also determine the length of time that the Unit 4 Turkey Point post-tensioning system will continue to" satisfy the Turkey Point licensing basis requirements. A report will be submitted to the NRC by January 29, 1993. (This report will be submitted as a Supplemental LER, only if the cause of the low lift-off condition differs from the cause stated in this LER.)
- 3. License amendments will be submitted to the NRC revising the design pressure of the containment buildings from 59 psig to 55 psig (Technical Specification 5.2.2 and BASES 3/4.6.1.4). These amendments will be submitted to the NRC no later than June 1, 1993.
V. ADDITIONAL INFORMATION No similar LERs have been identified.