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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:RO)
MONTHYEARML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6121997-08-29029 August 1997 LER 97-007-00:on 970730,automatic Reactor Trip Occurred. Caused by Closure of B Main Steam Isolation Valve.Failed W Relay & Equivalent Relays Were replaced.W/970829 Ltr ML17354A6081997-08-18018 August 1997 LER 97-006-00:on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power cabinets.W/970818 Ltr ML17354A5801997-07-14014 July 1997 LER 97-005-00:on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was reviewed.W/970714 Ltr ML17354A5141997-05-22022 May 1997 LER 97-002-00:on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons learned.W/970522 Ltr ML17354A5061997-05-0909 May 1997 LER 97-003-00:on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in drain.W/970509 Ltr ML17354A5051997-05-0909 May 1997 LER 97-004-00:on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were repositioned.W/970509 Ltr ML17354A4781997-04-25025 April 1997 LER 97-001-00:on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump tested.W/970425 Ltr ML17354A4581997-03-28028 March 1997 LER 97-002-00:on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning replaced.W/970328 Ltr ML17354A4511997-03-26026 March 1997 LER 97-001-00:on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was restored.W/970326 Ltr ML17354A4061997-02-0303 February 1997 LER 96-004-03:on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised ML17354A3771996-12-27027 December 1996 LER 96-012-00:on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log revised.W/961227 Ltr ML17354A3261996-11-0606 November 1996 LER 96-011-00:on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures revised.W/961106 Ltr ML17354A3071996-10-22022 October 1996 LER 96-010-00:on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors checked.W/961022 Ltr ML17353A8711996-08-27027 August 1996 LER 96-009-00:on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS.W/960827 Ltr ML17353A7411996-06-18018 June 1996 LER 96-008-00:on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures modified.W/960618 Ltr ML17353A7401996-06-18018 June 1996 LER 96-004-02:on 960524,identified Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Entered Tech Spec Statements,Tested Required Instruments Functions & Revised Plant procedure.W/960618 Ltr ML17353A6901996-05-13013 May 1996 LER 96-004-01:on 960220,identified Potential Tech Spec non-compliance Associated W/Surveillance Testing of AFW Actuation Circuitry on Sg.Caused by Inadequate Surveillance Procedures.Procedures revised.W/960513 Ltr ML17353A6741996-05-0606 May 1996 LER 96-001-00:on 960409,manual Rt Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion products.W/960506 Ltr ML17353A6651996-04-29029 April 1996 LER 96-007-00:on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being revised.W/960429 Ltr ML17353A6601996-04-25025 April 1996 LER 96-006-00:on 960327,manual Rt Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16.W/960425 Ltr ML17353A6491996-04-23023 April 1996 LER 96-005-00:on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 revised.W/960423 Ltr ML17353A6051996-03-18018 March 1996 LER 96-003-00:on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% power.W/960318 Ltr ML17353A6041996-03-18018 March 1996 LER 96-004-00:on 960220,surveillance Testing of AFW Actuation Circuitry Was Inadequate.Caused by Inadequate Surveillance Procedures.Tested Untested Portions of Actuation Logic for AFW Automatic Start signal.W/960318 Ltr ML17353A5861996-03-0606 March 1996 LER 96-002-00:on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B Sgfp Discharge Check valve.W/960306 Ltr ML17353A5761996-03-0101 March 1996 LER 96-001-00:on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned strainers.W/960301 Ltr ML17353A4451995-11-0909 November 1995 LER 95-007-00:on 951017,manual Rt Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water damage.W/951109 Ltr ML17353A4241995-10-12012 October 1995 LER 95-006-00:on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer tolerances.W/951012 Ltr ML17353A3601995-09-13013 September 1995 LER 95-005-00:on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train separately.W/950913 Ltr ML17353A2951995-07-17017 July 1995 LER 94-005-02:on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer ML17352B1581995-05-0505 May 1995 LER 95-004-00:on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies replaced.W/950505 Ltr ML17352B1181995-04-0707 April 1995 LER 95-003-00:on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers cleaned.W/950407 Ltr ML17352B0701995-03-13013 March 1995 LER 95-002-00:on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4.W/950313 Ltr ML17352B0321995-02-0909 February 1995 LER 94-005-01:on 941103,design Defect Found in Safeguards Bus Sequencer Test Logic,Placing Facility Outside Design Basis.Design Mods to Eliminate Software Logic Problems Will Be Implemented During Next Refueling outages.W/950209 Ltr ML17352B0101995-01-20020 January 1995 LER 94-006-00:on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire connection.W/950120 Ltr ML17352A9511994-12-13013 December 1994 LER 94-006-00:on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link checked.W/941213 Ltr ML17352A8871994-11-10010 November 1994 LER 94-005-00:on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI signal.W/941110 Ltr ML17352A8851994-11-10010 November 1994 LER 94-004-00:on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to automatic.W/941110 Ltr ML17352A8421994-10-21021 October 1994 LER 94-004-00:on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies reviewed.W/941021 Ltr ML17352A8431994-10-20020 October 1994 LER 94-005-00:on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket replaced.W/941020 Ltr ML17352B1671994-08-16016 August 1994 LER 94-003-00:on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr ML17354A7211997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Turkey Point,Units 3 & 4.W/971114 Ltr ML17354A7491997-10-13013 October 1997 SG Insp Rept. ML17354A8851997-10-13013 October 1997 FPL Units 3 & 4 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 960408-971013. ML17354A6801997-10-0808 October 1997 LER 97-008-00:on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens corrected.W/971008 Ltr ML17354A6791997-10-0606 October 1997 COLR Unit 4 Cycle 17, for Turkey Point ML17354A6811997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Turkey Point,Units 3 & 4.W/971009 Ltr 1999-09-30
[Table view] |
Text
AC CELLS RAYED DJSZKBUTI ON DEMONSTRATION SY~gM REGUDRTO INRORNA. ION DISTRIBUTION +TEN (RIDE)
~ACCESSION NBR:8807120057 DOC.DATE: 88/07/06 NOTARIZED: NO DOCKET FACIL:50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH. NAME AUTHOR AFFILIATION SALAMON,G. Florida Power & Light Co.
CONWA,W.F. . Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFZLIATION
SUBJECT:
LER 87-015-01:on 870715,Failure to deactivate inoperable containment isolation valve within 4 h,per Tech Specs.
W/8 S I U ION COD : 22D CO I S ECEZV D:LTR ~ E CL f SI E:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ZD CODE/NAME LTTR ENCL ZD CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2-2 PD 1 1 EDISONiG 1 1 INTERNAL: ACRS MICHELSON AEOD/DOA 1
1 ~
1 1"
ACRS MOELLER AEOD/DSP/NAS 2,2 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/QAB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/DREP/RAB 10 1 1 NRR/DREP/RPB 10 2 2 NRR D S SIB 9A 1 1 NUDOCS-ABSTRACT 1 1 CLEG 02 1 1 RES TELFORD,J 1 1 RES/DE/EIB 1 RES/DRPS DEPY 1 1 RGN2 FILE 01 1 EXTERNAL: EG&G WILLIAMSES 4 4 FORD BLDG HOYgA 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1
. NSIC MAYSEG 1 1 h
TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 44
UA. NUCLEAR REQULATORY COMMISSION N:1C Form 345 (543) APPROVED OMB NO, 31400104 EXPIRKS: 5/31/55 LICENSEE EVENT REPORT (LER)
DOCKET NUMBER (2) PA FACILITY NAME (1)
Turkey Point Unit 4 o s o o o 251 >oF 05 ai ure o eac iva e nopera e on asnmen so a son a ve 1 )n ours Required by Technical Specifications Due to Personnel Error EVENT DATE (5) LER NVMBKR (4) REPORT DATE (7) OTHER FACILITIES INVOLVED (4) inv'EQUENTIAL 5<<YA II4 VISION MONTH OAY YEAR FACILITYNAMES DOCKET NUMBERIS)
MONTH DAY YEAR R NUM44 tl 'cQ: NUMoote 0 5 0 0 0 0 7 1 5 8 7 7 015 01 07 06 8 8 0 5 0 0 Q THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS Of 10 Cf R f. (Coecp one or moro ol tnc lop~nfl (11)
OPERATINQ MODE (4) 20.402(4) 20.405(cl ~ 50.734) l2I()rl 73.7((4)
POWER 20.405( ~ I) I HO 50M(c) (I I 50.734)(2)(r) 73.71(cl LEYEL DTHER ldpeciry in 4ortrect 1 0 0 20A05( ~ l(1)IN) 50.34(c)(2) 50.73(el(2) (r4)
Oe/ow end in feet, NRC Fomr 20.405( ~ )(1)(SII 50.73(e)(2) (I) 50,73(e) (2)(rIBI(AI 366A) 20A05(e)11)(lr) 50.73(e l(2) I 4) 50.73 (e I (2) fr)5)(S I 20.405(e)() l(rl 50.'734)(2)(III) 50.73(e) 12) (r I LICENSEE CONTACT fOll THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Gabe Salamon, Compliance Engineer 305 24 6- 65 60 COMP(.ETE ONE I.INE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC TVRER REPORTABLE NPRDS <<o A'O
~
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<<Lope<<<<y . &i ': we CAUSE SYSTEM COMPONENT MANUF AC.
TURER EPORTABLE TO NPROS B D 8 4 M12 0 SUPPLEMENTAL RKPORT EXI'ECTKO (14 MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)
YES lllyer, complete EXPECTED SVdltlSSIOrt OATE) NO AINTRACT (Limit to ICOO epecee, l.e., epproepnetery lilteen rinprorpoco typerwttten lineel (ISI The solenoid for valve CV-956B was discovered to be causing a ground on July 13, 1987, with Unit 4 in mode 1. The valve was declared out of service (OOS), and the fuse was pulled, in compliance with Technical Specification (TS) 3.3.3, which requires isolation of each affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Following repair, power was restored and post~aintenance testing was performed with satisfactory results.
Inservice testing (IST) was completed at 0645, however local verification of valve position as required by procedure, was not performed. A new test was performed at 1805 on July 16, with satisfactory results. As the valve is OOS until completion of a satisfactory IST, valve CV-956B was OOS without complying with TS 3.3.3 between 0318, July 15, and 1805, July 16. The failure to perform the IST within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> was due to personnel error, in that the Shift Technical Advisor (STA) was not notified in a timely manner.
The IST performed at 0645 was also inadequate due to personnel error in that the STA failed to follow procedure OP 0209.1. Two additional instances of a failure to perform IST on a valve following maintenance, with similar. root causes, were identified. The root cause of the events was that the IST program had insufficient checks and balances to prevent a single personnel error from resulting in a missed IST.
8807120057 88070('3 P DR A DQCN O5OOOP 5 1 8 PNLJ NRC Form 345 r4 53 I
NR fons 3ddA U.S. NUCLEAR REQVLATORY COMMISSION
)943)
LICENSEE ENT REPORT (LER) TEXT CONTINU N APPAOVEO OMB NO. 3ISOW)04 EXPIRES: d/31/dd PACILITY NAME ll) OOCKET NUMSER IEI LEA NUMBER Id) PACE I3)
YEAR SEQVENTIAL REVISION
&54 NVMddR NVMddR Turkey Point Unit 4 o 5 o o o 2. 5-1 7 015 1 0 2 oF 05 TEXT lllmort t/rtct /t rtr)witr/, Irtt tr/I/R/orrt/HRC Fonrr Jr/rJA't/ )17)
The solenoid for valve CV-956B, the pressurizer liquid sample isolation control valve (EIIS:BD,KN), was discovered to be causing a hard ground on the 4B D.C. Bus on July 13, 1987, with Unit 4 in Mode 1. Upon discovery of the ground, the valve was declared out of service (OOS) and the fuse was pulled. This was performed in compliance with Technical .Specification 3.3.3, which requires that "with one or more of the isolation valve(s)... inoperable, maintain at least one isolation valve operable in each affected penetration that, is open and: a) restore the inoperable valve to operable status within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or b) isolate each affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> by use of at least one deactivated automatic containment isolation valve secured in the isolation position, or.... d) be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> ..." A Plant Work Order (PWO) was prepared and repair was initiated at 1530 on July 14. The PWO identified both post~aintenance (PM)>>testing and in-service testing (IST) as being required prior to returning the valve to service .
The cause of the ground was determined to be insulating tape which had deteriorated from normal aging. In the process of cleaning and retaping the connection, the power lead to the solenoid was lifted and then reterminated. Following the repair of the connection, the technician requested restoration of power and performed the required PM testing (cycling of the valve and verification of position indication) with satisfactory results . The fuse was reinstalled by a Reactor Control Operator (RCO) in accordance with .the above request 'at 2318 on July 14. Following cycling of the valve, the fuse was not pulled. At approximately 0630 on July 15, the RCO noticed that the valve was listed as being OOS in the Equipment Out of Service (EOOS) Log. He knew that the fuse had been reinstalled and the work completed.
He immediately realized that IST was needed and notified the Shift Technical Advisor (STA). The STA is the acting IST Coordinator when the plant IST Coordinator is not on site. The IST Coordinator is responsible for determining equipment post-maintenance IST requirements. IST of valve CV-956B requires cycling the valve, local and remote verification of valve position, and satisfactory timing of the valve stroke . The IST was completed at 0645, however local verification of valve position was not performed. The plant IST Coordinator, upon review of the above IST results, identified this discrepancy. A new IST, meeting all requirements, was performed at 1805 on July 16, with satisfactory results. As the valve cannot be considered to be in service until completion of a satisfactory IST, valve CV-956B was technically OOS without complying with the requirements of TS 3.3.3 between 0318, July 15, and 1805, July 16.
Two additional instances of a failure to perform IST on valves prior to returning them to service were discovered during later documentation reviews. The first instance occurred on June 13; 1987. Following maintenance on the actuator switch for valve CV-4-2821, the IST Coordinator should have been notified that the valve was ready for IST. The Plant Work Order indicated that the IST Coordinator was notified, however this could not be verified The next satisfactory IST was performed on September 8, 1987.
The second instance occurred on June 30, 1987. Valve CV-3-2819 was showing dual position indication upon actuation. The limit switches were ad]usted to indicate proper position. Following the ad)ustment, the STA, who was the acting IST NRC SORM dddA I4 431
NR Form 388A U.S. NUC(,EAR REOVLATORY COMMISSION (943)
LICENSEE NT REPORT (LER) TEXT CONTINU N APPROVEO OMS NO. 3150M)04 EXPIR ES: 8/31/88 FACILITY NAME (11 OOCKET NVMSER (2) LER NUMSER (8) PACE LS)
YEAR SEOV ENTIAL REVISION NVM ER NVM ER Turkey- Point Unit 4 /3 1 8'7 0 1 5 0 1 03 oF 0 5 TEXT ///moro Eooco /o oorr/rm/. vro or/didos HRC Fonrr 38SAS/ (IT)
Coordinator, was notified . *IST of the valve requires .cycling the valve, local and remote verification of valve position, and satisfactory timing of the valve stroke.
Post~aintenance testing of the valve was completed, however local verification of valve position and timing of valve stroke was not performed. Unit 3 was in mode 5 when the work was performed, and entered mode 4 on August 20, 1987 . The next satisfactory IST was performed on September 7, 1987.
CAUSE OP EVENT The CV-956B event has two deficiencies:,first, the failure to assure that the IST]
was performed within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> following restoration of power to valve CV-956B, and second, the failure to assure that post-maintenance IST requirements were met.
The cause of the failure to perform the IST within the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time limit is personnel error. Procedure AP 0190.28, "Postmaintenance Testing", requires the maintenance foreman/chief or supervisor to notify the IST Coordinator or the STA prior to commencing work. The STA was not notified until approximately seven hours after the fuse was reinstalled. Without receiving the required notification, scheduling the test in order to comply with the Technical Specifications was missed . Primary responsibility for assuring that LCO s are complied with rests with the Plant Supervisor-Nuclear . Even though he was notified via a temporary lift that the fuse was being reinstalled, no programmatic verification of any applicable LCOs was in place . Consequently, the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> LCO which was entered upon installation of the fuse was not emphasized and was missed.
The failure to assure that the initial IST was adequate was also due to personnel error in that the STA failed to follow procedure. Procedure OP 0209.1, "Valve Exercising Procedure", requires both local and remote position indication verification of valve CV-956B after maintenance, in addition to verifying the(
above every 2 years. In order to determine the acceptance criteria for the valve stroke time, the STA reviewed the results of previous tests, and noticed that the valve was tested within the last 2 years. The STA did not review OP 0209.1, which required local position verification after maintenance. As a result, he did not require this to be performed.
The root cause of the events was that the IST program had insufficient checks and balances to prevent a single personnel error from resulting in a missed IST.
The failure to perform IST of valve CV-4-2821 was inadequate communication following completion of work. At the time of this event, unit 3 was in mode 6, and unit 4 was in mode 5. With both units in modes 5 or 6, no STA is required to be on duty. This resulted in difficult communications and subsequent failure to identify the IST requirements'he failure to perform an adequate IST of valve CV-3-2819 was due to oversight by the STA, who was the acting IST Coordinator. The STA most likely did not review OP 0209.1, which required local position verification and valve stroke timing after maintenance . As a result, he did not require this to be performed .
NRC FORM SESA
/983)
NRC Fotm 344A'983)
U.S. NUCLEAR REOULATORY COMMISSION LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVEO OMS NO. 3)9)~IOO EXPIRES: 8/31/48 FACILITY NAME lll OOCKET NUMSER )3) LER NUMSER (4) PACE )3)
YCAR SCQUCNTIAL N9g ACV lt ION NUM Cll Kok NUMOCll Turkey Point Unit 4 o s o o o 8 7 -1 5 01 04 OF 05 TEXT ///moro tpocoit /oco/)od, oto oddidooo/I/RC Form 3////A'/ OT)
ANALYSIS OP EVENT One of the ways in which the release of fission products from the containment is limited is by the isolation of process lines by the Containment Isolation System (CIS). The CIS imposes double barriers in each line which penetrates the containment. While valve CV-956B was technically OOS during this event, it was capable of performing its design function had it been necessary. This was demonstrated by the initial PM test, and confirmed by the initial and final IST s.
Additionally, during the time that valve CV-956B was inoperable, the redundant containment isolation valve, CV-953, was operable.
While valve CV-4-2821 was technically OOS during this event, it was capable of performing its design function had that been necessary. This was confirmed by the regularly scheduled IST which was performed on September 8, 1987. No work was performed on this valve between June 13 and September 8, 1987.
While valve CV-3-2819 was technically OOS during this event, it was capable of performing its design function had that been necessary. This was demonstrated by the initial PM test which was performed on June 30, 1987, and confirmed by the regularly scheduled IST which was performed on September 7, 1987. No work was performed on this valve between June 30 and September 7, 1987.
Based on the above, the health and safety of the public were not affected.
CORRECTIVE ACTIONS The following corrective actions were taken in order to centralize control of post-maintenance IST and to add checks to assure completion of IST prior to the return of equipment to service:
- 1) Valves CV-4-956B, CV-4-2821, and CV-3-2819 were in-service tested with satisfactory results .
- 2) Procedures AP 103.2, "Responsibilities of Operators and Shift Technicians on Shift and Maintenance of Operating Logs and Records," AP 190.19, "Control of Maintenance on Safety Related and Quality Related Systems," and AP 190.28, "Post Maintenance'Testing," were revised to assure that )the IST Coordinator or STA is notified prior to the initiation of work which will involve IST components.
- 3) Procedures 3/4-GOP-503, "Cold Shutdown to Hot Standby," and 3/4-GOP-301, "Hot Standby to Power Operation," were revised to require the IST Coordinator or STA to verify that all required IST has been completed prior to a mode change .
- 4) Procedure O-ADM-502, "In-Service Testing (IST) Program," was generated to centralize the requirements for all IST in one procedure .
- 5) Procedure AP 103.4, "In-Plant Equipment Clearance Orders," was revised to require the STA or the IST Coordinator to be named as a clearance holder for all clearances on IST components.
NRC SO/)M 344A Io All
NRC PoNR (SEA US. NUCLEAR REGULA'TORY COMMISSION I
((L(LII LICENSEE lNT REPORT (LERI TEXT CONTINU~N APPROVEO OMS NO, 3150W104 EXPIRESI 8/31/88 PACILITY NAME (ll OOCKET NUMBER (3( LER NUMSER (el PAGE (31 YEAR SEOUENTIAL REVISION NVMSER NUMEER Turkey Point Unit 4 o s o o o 2 5 1 8 7 0 I 5 01 05 OF 0 5 TENT //awe <<>>ee N IEEMSSIE NPP /SNand N/IC %%d/IR 3(ISAE/ (IT(
- 6) Procedure O-ADM-701, "Plant Work Order Preparation," was revised to require STA or IST Coordinator notification, and to require the Operations Maintenance Coordinator to review post-maintenance testing and IST requirements for Technical Specification Limiting Condition of Operation and Mode applicability.
~
ADDITIONAL DETAILS CV-4-956B Valve Operator Manufacturer: Masoneilan International, Inc. Operator Model Number: 38-2057.
Similar occurrences: LER s 251-85-23, 251-86-24 NRC EORM seeA RU S.GPO:Ieeb4 834 538/455 (8$ 3 I
JULY 0 6 1980 L-88-266 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Reportable Event: 251-87-15 (Revision 1)
Date of Event: July 15, 1987 Failure to Deactivate Inoperable Containment Isolation Valve Within 4 Hours as Required by Technical S ecifications Due to Personnel Error The attached Licensee Event Report revision is being submitted to discuss two previous incidents found during a recent documentation review. Our original report was issued August 14, 1987 in FPL letter L-87-332.
A two week extension on the submittal of this LER was requested of and granted by the NRC Region more time to analyze the root cause II Staff to allow and take proper corrective actions.
Very truly yours, W. . Conw Senior Vice President Nuclear WFC/SDF/gp Attachment cc: Dr. J. Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant SDF3Rev1.LER