ML17326A749

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Forwards LER 80-022/03L-0
ML17326A749
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 10/01/1980
From: Shaller D
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A750 List:
References
NUDOCS 8010080403
Download: ML17326A749 (4)


Text

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++leotr la y t INDIANA & MICHIGAN EIECTRIC COMPA N Y DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 (616) 465-5901 October 1, 1980 Mr. J.G. Keppler, Regional Director Office of Inspection and Enfor'cement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315

Dear Mr. Keppler:

Pursuant to the requirements of the Appendix A Technical Specifications, the following report/s are submitted:

RO 80-022/03L-O.

Sincerely, D.V. Shaller Plant Manager

/bab cc: J.E. Dolan R.S. Hunter R.W. Jurgensen R.F. Kroeger R.W. Kilburn E. Swanson/N. DuBry RO:III R.C. Callen MPSC G. Charnoff, Esq.

G. Olson J.M. Hennigan W. Lavallee EPRI PNSRC J.F. Stietzel E.L. Townley Dir., IE (30 copies) @DE Dir., MIPC (3 copies) St (

C.

4'

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7.77~'I' LICENSEE EVENT REPORT CONTROL BLOCK: QE (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6 0 1 M I D C C 'OE 0 0 0 0 0 0 0 0 003" 25 26 LICENSE TYPE 104~OR 30 57 CAT 58 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER CON'T

~O soURGE LLJO 0 5 0 0 0 3 1 68 Q 69 0 0 EVENT DATE 6 8 OQB

'74 75 1 0 0 1 REPORT DATE 8 0Q 80 7 8 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 010 DURING NORMAL OPERATIONS, A LOW FLOW ALARM WAS RECEIVED ON RADIATION MONITORS

~03 R-ll/R-12'ONSTITUTING AN INOPERABLE MONITOR PER TECH. SPEC. 3. 3. 3. 1. ACTION 4 REQUIREMENTS WERE MET. THE PUBLIC HEALTH AND SAFETY WERE NOT AFFECTED BY THIS 6 EVENT. SIMILAR EVENTS INCLUDE 79-012/03L-O, 79-048/03L-0; AND FOR DOCKET 050-6 316'9 034/03L 0 AND 80 018 013/03L 0

~O7

~08 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OB 8 9

~BB 10 Q77 11 E QEE ~BQ73 12 13 P U M P X X Q4 18

~MOPE 19

~Z 20 O

7 SEQUENTIAL OCCURRENCE REPORT REVISION Q

LER)RP REPQRT ACTION FUTURE EVENT YEAR

~80 21 22 EFFECT

~

23 SHUTDOWN

~02 24 REPORT NO.

2 26

~W 27

~03 28 ATTACHMENT CODE 29 NPRDQ TYPE

~L 30 PRIME COMP.

31 NO.

32 0

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS +22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~AO78 ~CQ78 ~ZQ2D ~ZQ2i 0 0 0 11 ~NO23 ~NQ>4 ~AO28 W 1 2 0 P2.

33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE'ACTIONS Q27 o THE INOPERABILITY WAS CAUSED BY A FAILED LOVEJOY L-100 SHAFT COUPLING. THE COMPLETE COUPLING WAS REPLACED AND THE AIR MONITOR WAS TESTED AND DECLARED OPERABLE WITHIN 8 HOURS. PRESENT PLANS ARE TO REPLACE THE ENTIRE R-ll/R-12 SYSTEM AS A PART OF DES IGNCHAhSE1 2-2448 ~

3 4

80 7 8 9 FACILITY ~3P METHOD OF STATUS 5 POWER OTHER STATUS PQ DISCOVERY DISCOVERY DESCRIPTION 8 ~E Q28 ~10 10 0

12 Q28 13 N/A 44

~A 45 Q31 46 RESPONSE TO AN ALARM 80 8 9 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITYQ36 LOCATION OF RELEASE Q

~s 7 8

~ZO33 9

~ZO 10 N/A 45 N/A 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~l7 ~00 0 Q37 ~Z 12 Q38 13 N/A 80 7 8 9 11 PERSONNEL INJURIES NUMBER DESCRIPTIONQ

~OO O Q48 N/A 8 9 11 12 80 7

LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION Z Q4, N/A ~ j&egdS"z~

8 9 10 80 PUBLICITY NRC USE ONLY ISSUED DESCRIPTION

[22O] ~NQ44 N/A 10 68 69 80 ER 8 9 NAME OF PREPARER PHONE,(6 16) 465-590 1 EXT ~ 1 036

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