ML17164B002

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Insp Repts 50-387/99-02 & 50-388/99-02 on 990119-29.No Violations Noted.Major Areas Inspected:Engineering & Aspects of Util Corrective Action Program & Response to GL 96-01
ML17164B002
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 04/05/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17164B001 List:
References
50-387-99-02, 50-387-99-2, 50-388-99-02, 50-388-99-2, GL-96-01, GL-96-1, NUDOCS 9904120212
Download: ML17164B002 (33)


See also: IR 05000387/1999002

Text

U.S. NUCLEAR REGULATORYCOMMISSION

REGION I

Docket Nos:

License Nos:

50-387, 50-388

NPF-14, NPF-22

Report No.

50-387/99-02, 50-388/99-02

Licensee:

Pennsylvania Power and Light Company

2 North Ninth Street

Allentown, Pennsylvania

19101

Facility:

Susquehanna

Steam Electric Station

Location:

P.O. Box 35

Berwick, PA 18603-0035

Dates:

January 19 through January 29, 1999

Inspectors:

R. Fuhrmeister, Senior Reactor Engineer

G. Morris, Reactor Engineer

D. Vito, Senior Allegation Coordinator

Approved by:

Lawrence T. Doerflein, Chief

Engineering Programs Branch

Division of Reactor Safety

9904120212

990405

PDR

ADOCK 05000387

8

PDR'

I

EXECUTIVE SUMMARY

Susquehanna

Steam Electric Station (SSES), Units 1 8 2

NRC Inspection Report 50-387/99-02, 50-388/99-02

This inspection included aspects of Pennsylvania Power and Light Company's (PP8L's)

corrective action program and PP8L's response to NRC Generic Letter 96-01.

~En ineeiin

The inspector concluded that PP8L's response to Generic Letter 96-01 adequately

addressed

the issues identified in the GL, and that there was an adequate

basis for the

positions taken in the response.

(Section E1.1)

The inspectors concluded that the surveillance testing procedures reviewed

satisfactorily met the testing requirements outlined in NRC Generic Letter 96-01.

The inspectors also determined that the minor discrepancies

noted in the procedures

and drawings would not have affected the outcome of the testing.

(Section E2.1)

The inspector determined that the procedures for control of modifications to the

facility provided appropriate controls for ensuring that modifications were properly

carried over into the technical specifications and surveillance tests.

(Section E3.1)

The condition report (CR) process

is a high volume, low threshold corrective action

system that is acceptable to meet the requirements of 10 CR 50, Appendix B,

Criterion XVI. Adverse conditions are promptly identified and the process appears

to be widely accepted for use, and is used by a broad cross section of the plant

staff. There are no significant delays in the initial assessment,

investigation, and

completion of initial operability and reportability determinations.

Initial investigations

and root cause assessments

for issues of higher safety significance are thorough.

Investigations and causal analyses for CRs of lesser safety significance are generally

thorough, but there are some instances where extent of conditions and/or generic

implications may not be sufficiently explored.

(Section, E7.1)

The condition report process

is focused on accomplishing initial reviews,

reportability and operability determinations,

cause assessments,

and establishment

of proposed corrective actions to correct the condition and prevent recurrence.

However, process accountability is not readily apparent

in the corrective action

implementation portion of the process.

Corrective action implementation dates do

not correlate with the assigned significance level. Action due dates are controlled

by the responsible manager who may change them during the course of

implementation. The only procedural requirement regarding corrective action

implementation is refueling outage related with the shortest lead time being

approximately 7-'10 months, and the longest lead time being approximately 31-37

months.

The minimal administrative control over the corrective action

implementation portion of the process contributes to a high process backlog.

(Section E7.1)

Executive Summary (cont'd)

~

Internal reviews of the condition report system by Operating Experience Services

(OES) and external reviews by Nuclear Assurance Services (NAS), the Cooperative

Management Audit Program, the Institute of Nuclear Power Operations, and the

Susquehanna

Review Committee are continuing to find incomplete or inadequate

corrective action closure.

A recent process change requiring OES to review

competed'actions

to ensure that the actions satisfies the one prescribed,

is reducing

the amount of items identified. However, problems persist in this area.

(Section

E7.1)

Annual assessments

of the condition report process by NAS were thorough, critical,

and well founded.

NAS assessments

conducted in 1997 and 1998 identified most

of the concerns identified by the inspectors.

(Section E7.1)

.

TABLEOF CONTENTS

EXECUTIVE SUMMARY..

TABLEOF CONTENTS

.IV

III. Engineering

.

E1

Conduct of Engineering

.

E1.1

Response to NRC Generic Letter 96-01

.

E2

Engineering Support of Facilities and Equipment

E2.1

Functional Testing of the Diesel Generator "C" Starting Circuits

E3

Engineering Procedures and Documentation

E3.1

Modification Process Procedures

..

. 3

.3

E7

Quality Assurance in Engineering Activities

E7.1

Corrective Action Program

.

V.

Management Meetings

X1

Exit Meeting Summary

.

16

16

Re ort Details

III. En ineerin

E1

Conduct of Engineering,

E1.1 'es

onse to NRC Generic Letter 96-015

5 251

92

To assess

the adequacy of the Pennsylvania Power and Light (PP8L) response to NRC Generic Letter (GL) 96-01, the inspector reviewed PP8L's response,

dated

April 18, 1996, Licensee Event Reports (LERs) for 1996, 1997, 1998, and Condition

Reports (CRs) for those LERs from the selected period which identified inadequate

testing.

b.

Observations and Findin s

Industry Experience Review Program Action Item (IERP) No. 96007 was opened on

January 19, 1996, to track PP8L actions in response to the. generic letter. The IERP

developed two recommended

actions based on a review of the Surveillance Program

Task Force activities in 1984. The recommendations

were to upgrade the highlighted

drawing system and to revise the surveillance test program implementing procedure to

incorporate the testing philosophy develop'ed by the task force in 1984. The PP8L

'esponse

to GL 96-01 stated that the requirements of'the GL had been met since the

surveillance testing procedures for the Susquehanna

Steam Electric Station (SSES) are

in compliance with the Units'echnical Specifications.

This conclusion was based upon

having performed a review of surveillance testing during the startup testing of Unit 2 in

the 1984 time frame and having an ongoing program to ensure that modifications are

properly tested and incorporated into surveillance tests.

Additional reviews of testing

were not conducted at the time of the response.

9

During the time period 1996 through 1998, seven LERs identified inadequate

surveillance testing of safety related circuits. Two of these were related to response time

testing, and were, therefore, outside the scope of the activities requested

by the generic

letter. CRs generated

by PP8 L to address the issues identified in the other five LERs

were reviewed to determine what corrective actions PP8L had implemented and the

extent of the conditions.

LER 50-387/98-12, which was also applicable to Unit 2, documented that the testing of

the suppression

pool temperature monitoring instrumentation did not meet the

requirements for a logic system functional test of the alarm function of the instruments.

This condition was evaluated under CR 98-1972.

PPBL determined that past tests

actually only performed a channel calibration. Alternative testing to meet the channel

functional test requirement was identified and approved by the plant operations review

committee (PORC).

The CR identified four other CRs which identified occasions where it

was discovered that the surveillance tests did not properly implement surveillance

requirements.

The evaluation of the five deficiencies in total concluded that there was no

significance since-"These errors represent 0.5% (10 of 2000) of all the station's

surveillance procedures."

LER 50-387/98-10, which was also applicable to Unit 2, documented that the main

feedwater turbine and main generator turbine trips on reactor vessel high water level

were not adequately tested.

This condition was documented in CR 98-0697. The testing

was carried out by use of overlapping tests, which it turns out, did not test the final

outputs to the trip function. The final output device was in fact tested, but the test was

not called out for satisfying the surveillance requirement.

This CR developed a time line

for the test methodology, which showed that this problem was first identified during the

surveillance testing review. in 1984. Corrective actions at the time included a procedure

change; however, it was not incorporated into the next procedure revision. The licensee

plans to revise the procedures to correct the discrepancy prior to the next required test.

LER 50-387/98-04 documented a failure to test portions of the residual heat removal

(RHR) pump start logic. This condition was evaluated under CR 98-0427 and 98-0528,

which determined that the power monitor relays for all four pumps in both plants had not

been tested.

Test procedures were revised and the relays were satisfactorily tested.

In

response

to this condition, several other systems were reviewed to determine ifsimilar

conditions existed.

No similar problems were identified in the other systems.

An

additional corrective action was assigned to evaluate the need to revise or supplement

the PP&L response to GL 96-01.

PP&L determined that a supplement was warranted,

and tracking item E20235 was generated to ensure completion of the supplemental

response.

A due date of September

1, 1998, was originally assigned.

At the time of this

inspection, the due date had been previously'extended to January 29, 1999. At the end

of the inspection, the due date was again being extended, with completion expected in

mid- to late February, 1999.

Conclusions

The inspector concluded that PP&L's response to Generic Letter 96-01 adequately

addressed

the issues identified in the GL, and there was an adequate basis for the

positions taken in the response.

Engineering Support of Facilities and Equipment

Functional Testin

of the Diesel Generator "C" Startin

Circuits

Ins ection Sco e (IP Tl 2515/139)

The team reviewed selected portions of control logic drawings, schematic diagrams, and

surveillance test procedures to assess

the completeness

of PP&L's logic system

functional testing.

/

b.

Observations and Findin s

The inspectors reviewed the surveillance tests associated with the Division I Loss of

Offsite Power (LOOP) and Loss of Coolant Accident / Loss of Offsite Power

(LOCNLOOP) initiated starting of the "C" diesel generator and loading to the Unit 1 4.16

kV Bus 20301.

In 1998, PP8L had completely revised the Unit 1 surveillance test

procedures to incorporate the changes

in the surveillance test requirements which

resulted from the approval of the Susquehanna

Steam Electric Station (SSES) Improved

Technical Specifications (ITS), and to incorporate the 24 month operating cycle. The

surveillance procedures which the inspectors reviewed were clear and well written.

PP8L uses multiple overlapping procedures to test the complete circuits covering the

LOOP and LOCNLOOP logic from the initiating instrumentation to the diesel start, bus

load shedding, load sequencing and bypass of the diesel generator non-essential

protective trips for each diesel, each unit, and each division. The procedures

satisfactorily tested the portions of the circuits reviewed by the inspectors.

The

inspectors found only minor errors in several of the procedures and drawings where

associated

schematic drawings were incorrectly referenced (for information only) and

which did not affect the implementation nor the results of the test procedures.

Minor

technical discrepancies

between the surveillance procedures and the Final Safety

Analysis Report (FSAR) had already. been identified by PP8L, had been processed

through their condition report program and a licensing document change notice (LDCN)

had been issued to correct the FSAR.

The team observed that PP8 L did not test the active protective trips of the diesel

generator (generator differential overcurrent, engine overspeed,

and low lubricating oil

pressure) during operation in the emergency mode.

During discussions with the

Improved Technical Specification group in the Office of Nuclear Reactor Regulation

(NRR) the inspectors confirmed that testing these three protective trips is not specifically

required by ITS Surveillance Requirement 3.8.1.13.

b.

Conclusions

The inspectors concluded that the surveillance testing procedures reviewed satisfactorily

met the testing requirements outlined in NRC Generic Letter 96-01. The inspectors also

determined that the minor discrepancies

noted in the procedures and drawings would not

have affected the outcome of the testing.

E3

E3.1

Engineering Procedures and Documentation

Modification Process Procedures

The inspector reviewed procedures which control the design and installation of

modifications at SSES, to determine how modification information is carried over into the

technical specifications and surveillance test procedures.

Observations and Findin s

Nuclear Department Procedure MFI-2309, Rev. 6, "DCP/ECO Preparation Instructions,"

provides "how-to" instructions for preparing items associated

with Design Change

Packages

(DCPs) and Engineering Change Orders (ECOs). The procedure specifies

that appropriate testing strategies, methods, specifications, parameters

and acceptance

criteria be developed during the preliminary design phase.

The modification, its design

and installation are to be developed by a team of personnel, whose specialties address

needs identified in the modification scoping report.

Nuclear Department Instruction MFI-3203, Rev. 1, "Guidelines for Installation Kickoff

Meeting (IKM),"outlines responsibilities for personnel attending the IKM,which must be

held prior to issuance of each plant modification package (PMP). The procedure

provides guidance for developing installation and testing strategies, and assigns the

associated

system engineer the responsibility for determining ifthe modification affects

other systems, nuclear instrumentation, thermal power heat bala'nce inputs, and whether

any procedure changes are required as a result of the modification.

ti

NDAP-QA-1211, Rev. 3, "SSES DCP/ECO Installation Process," ensures that the

installation process for DCPs and ECOs is performed in a consistent, controlled, and

documented manner.

The procedure covers such activities as providing input to the

Engineering Integrated Schedule, preparing the PMP, ordering material, monitoring

installation.and testing, resolving installation problems, and closeout activities. Design

activities are specifically excluded, since they are covered by a separate procedure.

The

procedure also'requires a review of the modification design ifinstallation is delayed more

than thirty months.

This review is intended to ensure that the modification complies with

the current design and licensing basis of the plant. These reviews are conducted on a

case-by-case

basis for delays less than thirty months.

MFP-QA-3904, Rev.1, "Digital Control Scheme Testing," establishes

a standard method

of performing and documenting digital control scheme post modification inspections and

testing for DCPs and ECOs. The procedure requires, among other things, systematic,

thorough, contact-by-contact, conductor-by-conductor continuity checks of the modified

scheme, as shown on the designated drawings prior to energizing the circuit. The

procedure requires the testing to go one point beyond the modified wiring ifpractical, into

the circuitry outside the scope of the DCP/ECO. The requirements for energized testing

of the modification include identifying each logic path configuration, verifying proper

functioning of all contacts (both opening and closing), and testing each path to the end,

including operating initiation devices.

Improved Technical Specifications, license amendment

1?8 for Unit 1 and 151 for Unit 2,

defines a channel functional test as the injection of a simulated or actual signal into the

channel as close as practical to the sensor, and verifying operation of all required

alarm,'nterlock,

display, trip and channel failure trip functions. The definition allows testing to

be performed by sequential, overlapping steps, as well as total channel tests.

I

c.

Conclusions

The inspector determined that the procedures for control of modifications to the facility

provided appropriate controls for ensuring that modifications were properly carried over

into the technical specifications and surveillance tests.

E7

Quality Assurance in Engineering Activities

E7.1

Corrective Action Pro ram (IP 40500)

To evaluate PP8L's program for identifying and correcting conditions adverse to quality,

the inspectors reviewed the site procedures governing identification and correction of

adverse conditions and corrective action system files selected at random, both open files

and files which had been closed within the previous year.

b.

Observations and Findin s

At SSES, the Condition Report (CR) process is the predominant means of identifying,

documenting and correcting conditions adverse to quality. The CR process is a high

volume, low threshold problem reporting system, which in addition to plant safety issues,

may also include site issues that are not specifically related to nuclear safety.

Th'

current CR process has been in place since 1996, when it replaced several separate

processes

that tracked issues in various functional areas (daily operational issues,

quality assurance

issues, radiological controls issues, industry experience issues, etc.).

The current process encompasses,

but is not limited to, the following types of concern:

daily operational and maintenance concerns

quality assurance

audit and surveillance findings

industry experience issues

issues identified by PP8L site engineering

issues identified by PP8L corporate engineering

Institute of Nuclear Power Operators (INPO) issues

NRC generic correspondence

other concerns and requests for information referred to PP8L by NRC

procurement issues (ifnot caught by the receipt inspection program)

technical issues referred from the SSES Employee Concerns Program (ECP)

programmatic and human performance issues related to health physics and

radiological controls

issues identified due to apparent trends from previously identified CRs

issues identified due to incomplete or incorrect corrective actions from previous

CRs

The CR process does not include industrial safety issues (although some significant

industrial safety issues may be included in the CR process).

The inspectors reviewed the current CR procedure (NDAP-QA-0702), and the current

versions of the following procedures which denote interface with the CR process:

NDAP-QA-0703 - Operability Assessments

and Requests for Enforcement Discretion

NDAP-QA-0720 - Station Reporting Matrix and Reportability Evaluation Guidance

NDAP-QA-0721- Human Performance Evaluation System (HPES)

NDAP-QA-0730 - Controlling Changes to Licensing Documents

NDAP-QA-0726 - Safety Evaluations

NDAP-QA-0300 - Conduct of Operations

NDAP-QA-0502 - Work Authorization System

NDAP-00-0109 - Nuclear Safety Concerns of Individuals

OES-AD-001 - Condition Report Processing/Event

Trending

The inspectors obtained and reviewed a summary listing of currently open CRs and a

listing of all CRs closed in calendar year 1998.

From the summary listings, the

inspectors selected and performed a detailed review of 45 CR files (17 closed files and

28 currently open files). The inspectors discussed aspects of the CR process and the

specific CRs reviewed with several members of the SSES plant staff from various

functional departments.

Process Guidance and Trainin

The CR procedure (NDAP-QA-0702) underwent a major revision in September 1998.

The most notable changes include the following:

The procedure clarified the role of Operations in initial operability/reportability

assessments,

to assure that Shift Supervision performs operability/reportability

determinations promptly when appropriate.

The licensee indicated that in the

past, there had occasionally been delays in obtaining initial

operability/reportability assessments

for CRs that were not submitted directly to

Operations.

The procedure added a requirement for Operating Experiences Services (OES),

the department that administratively tracks the CR process, to review completed

actions to ensure that the action taken satisfies the action prescribed.

This

function was instituted due to a persistent process problem which, due to a lack

of contemporaneous

corrective action implementation review, resulted in

numerous issues being revisited because of corrective action being either

inadequate,

incomplete, or not being performed at all.

The procedure added a new requirement for an "effectiveness review" to be

performed for CRs of higher significance, to obtain a more prompt assessment

of

the effectiveness with which more significant concerns are resolved, and to

evaluate whether the actions taken were successful in preventing or significantly

reducing the potential for recurrence of the initial event. At the time of the

inspection, none of these effectiveness reviews had been completed, so none

were available for review.

It should be noted that the effectiveness review will

also affect the overall timeliness for CR closure since it is intended that affected

CR files will not be closed until the effectiveness review is complete.

The CR procedure and other related procedural guidance is relatively clear and easy to

follow. Forms are provided for documentation of the problem, the operability and

reportability assessments,

the root cause or causal analysis, the initial investigation into

the matter, past experience, additional safety assessments,

proposed actions to correct

the problem and prevent recurrences,

Human Performance Evaluation System (HPES)

information, and assignment of corrective actions.

The process is being implemented

as described in the procedure and appears to get wide use.

Regarding the recent full re-write of the CR procedure, each functional group was

provided a training package to brief their staff on the new procedure.

New employees

are provided training on the CR process during their initial indoctrination. OES also

provides periodic update training to engineering personnel at the PP8L corporate office

in Allentown. Also, the OES Supervisor issues periodic electronic mail messages

to the

site staff to discuss changes and enhancements

to the process.

Recent focus is'on the

implementation of the SSES electronic database,

the Nuclear Information Management

System (NIMS), and the services it willmake available to the PP8 L staff regarding CR

activities and status.

Process

Im lementation/ WorkfIow

CR Initiation and Initial Assessment

The CR process applies to the entire site staff and also to personnel in the PP8L

Corporate Office who interface with SSES personnel and activities. Employees are

encouraged to submit Condition Reports through their supervisor, but this is not

specifically required.

This is acceptable since an employee may, in some cases, feel

apprehensive

about having to obtain his/her supervisor's acceptance

before a concern is

submitted.

The inspectors noted that CRs were submitted through the supervisor in the

large majority of cases.

Based on the number of CRs submitted, and the large variety and variability of concerns,

the process appears to be widely accepted for use, and is used by a broad cross section

of the PP8L staff.

Ifan employee wishes to remain confidential, he/she may report their

concern through the Employee Concerns Program (ECP).

Ifappropriate, ECP willfile

the employee's technical issues with the CR process and provide feedback to the

individual with regard to the resolution of each issue.

The inspectors discussed this

aspect of the process with the site ECP manager, who indicated that the number of ECP

issues that he has had to channel through the CR process has been minimal, and that

there has not been a problem with providing feedback to individuals who channel their

technical concerns through ECP.

There is no specific requirement to provide feedback

to those individuals who file CRs through the normal process.

CR issues that may impact plant operations, the plant Technical Specification, or the

SSES Technical Requirements Manual are to be provided to Shift Supervision so that

initial operability/reportability assessment

may be performed.

Ifa CR is submitted to

OES before it is presented to Operations, OES assures that the CR is provided to

Operations promptly so that initial operability/reportability assessment

may be

performed.

Upon receipt, CRs are processed

through OES for initial screening and establishment

in

the tracking database.

An initial screening meeting is held within OES within a day or

two of the receipt of the CR at which a significance level is assigned to each CR.

Significance is assigned as follows:

Level 1 - Significant and Consequential

Level 2 - Significant or Consequential

Level 3 - Low Significance and Low Consequence

Level 4- Precursor or Minor

The OES screening meeting is attended by the OES Supervisor and his evaluation staff,

and often includes representatives

from the Operations and Maintenance departments to

provide additional insight into the issues raised.

The OES Supervisor indicated that his

department has made a concerted effort over the past year to categorize CRs

appropriately, since in the past, significance levels may have been assigned too

conservatively.

In particular, the OES Supervisor indicated that many issues that should

have been categorized as Level 3, were categorized as Level 2, requiring more

evaluation and effort, and contributing to the already high backlog. Current efforts in

assigning significance levels appear to be appropriate and consistent with the procedure.

In addition to the assignment of a significance level, the OES screening meeting

determines the responsible manager, attempts to identify any apparent causes or causal

factors, and whether any interim corrective actions may be appropriate before longer

term corrective actions are proposed by the responsible manager.

The screening

meeting also evaluates whether any specific equipment failure constitutes a

Maintenance Rule functional failure.

The OES screening meeting also attempts to determine whether a given CR describes

an event similar to a previous event or events, or has similar causes to those of previous

events.

Ifso, OES may consider initiating a new CR to demonstrate the existence of an

adverse trend.

OES bases its decision to open a "trend",CR on the knowledge of the

OES staff with regard to previous CRs that have been, received.

"Trend" CRs may also

be initiated as a result of findings made by other assessments

of the corrective action

program (QA audits and surveillances, INPO, etc.). The inspectors noted that there are

no formal criteria to establish what is or is not an adverse trend, and there is no

structured method of performing periodic trending. The OES supervisor acknowledged

that with the'recent inclusion of CR database

information on the Nuclear Information .

Management System (NIMS), the opportunity is available to develop more formalized

trend analysis and reporting capabilities.

The OES Supervisor has recently assigned a

staff member to develop electronic trending capabilities.

Within a day or two of the OES screening meeting, a CR is scheduled for discussion at

the daily Corrective Action Team (CAT) Meeting.

The CAT meeting is attended by

higher level managers from the site functional departments

and OES personnel.

Corporate engineering is telephonically linked. At the CAT meeting, OES personnel

present Level 1 and Level 2 CRs and the results of the initial OES screening of those

CRs.

Comments and changes are incorporated into the CR by OES.

Level 3 and Level

4 CRs are not discussed at the CAT meeting unless questions are asked by meeting

attendees.

Afterthe CAT meeting, Level 1 and Level 2 CR packages,

and Level 3 CR packages for

which an evaluation is required are issued to the responsible manager, who will

determine the course of action to resolve the CR and prevent its recurrence, ifpossible.

At this point in the process, the responsible manager develops the investigative

documentation for each CR as required by NDAP-QA-0702, and puts together the

Evaluation and Action Plan (E8AP). Level 1 CRs require an investigation into the

concern, a safety assessment,

a root cause assessment,

an assessment

of causes and

causal factors, and development and assignment of corrective actions.

Level 2 CRs

require a similar review to Level 1 CRs, but only require an assessment

of apparent

cause versus a root cause assessment.

For Level 3 CRs requiring an evaluation, an

investigation is performed and causes and causal factors are assessed,

in addition to the

development and assignment of corrective actions.

For Level 3 CRs which simply

require that the noted condition be corrected, OES inputs the actions derived at the OES

screening meeting to the CR electronic database,

and assigns them to the responsible

manager.

The responsible managers must complete the initial evaluation of a CR and

determine the corrective actions to be completed according to the following schedule:

20 calendar days from the event date for Level 1 and 2 CRs involving reportable

or potentially reportable events

30 days from the CAT meeting for all other Level 1 and 2 CRs

120 calendar days for Level 3 CRs

CR Corrective Action lm Iementation

While the timeliness of developing the E8AP is correlated with the CR significance level,

the implementation of corrective actions is not. NDAP-QA-0702 describes the

development of the EBAP as the point of resolution of a CR. However, the deficiency is

not actually resolved at this point, as corrective actions have yet to be implemented.

The

completion dates for corrective actions are developed and assigned by the responsible

manager.

The responsible manager may change the due date of a given corrective

action at his/her prerogative during the course of its implementation.

The only

procedural requirement regarding the implementation of corrective actions is refueling

outage related.

Generally, corrective actions for CRs are assigned to the next refueling

outage which starts greater than 6 months from the event date.

For CRs affecting both

units, corrective actions are assigned to the refueling outage with the longest lead time.

In other words, the shortest lead time for implementing a CR corrective action would be 6

months plus the duration of the next refueling outage, (plus an additional month if

completion of a specific CR is not a requirement for restart).

The longest lead time for

10

implementing a CR corrective action could be 30 months (assuming a 24-month

operating cycle) plus the duration of the next two refueling outages (plus an additional

month ifcompletion of a specific CR is not a requirement for restart).

Ifthese

completion times cannot be met, extensions must be approved by the General Manager-

SSES and the General Manager - Nuclear Engineering.

These requirements do not

apply to the completion of modifications. The lack of administrative control over the

corrective action implementation portion of the CR process appears to be a significant

contributor to corrective action timeliness issues and the overall CR backlog. Of the

'690 CRs open at the beginning of the inspection, 2.3 % were greater than 2 years old

(including 3 Level

1 and 30 Level 2 CRs), 23+% were greater than

1 year old, and 53+%

were greater than 6 months old.

Since December 1998, some site managers

have implemented internal departmental

requirements that CR action due date extensions be negotiated and approved by the

responsible manager before the date can be changed in the database.

While this

appears to have imparted some degree of additional accountability into the process, the

cycle end date remains as the only established requirement for completion.

CR Closure

After corrective actions have been implemented, OES reviews the CR package to ensure

'hat implemented corrective actions are commensurate with those prescribed.

Ifa

corrective action is incomplete or inappropriate, OES refers it back to the responsible

manager for reassessment

and resolution. This aspect of the process was initiated in

October 1997, due to a persistent process problem which, due to a lack of

contemporaneous

corrective action implementation review, resulted in numerous issues

being revisited because of corrective action being either inappropriate, incomplete, or not

being performed at all.

When these reviews were initiated, OES indicated that a "reject

rate" of 15+% was encountered.

The efforts and oversight provided by OES for this

function over the past year have reduced the "reject rate" considerably, to less than 2%.

This effort notwithstanding, problems with corrective action implementation continue to

be identified by sources external to OES (QA, INPO, etc.). At the beginning of the

inspection, there were 34 open CRs related to inappropriate or incomplete completion, of

CR corrective actions.

Once the corrective actions are determined to be complete, OES closes out the CR in

the NIMS database.

CR Trendin

Trending capability is an important aspect of a corrective action program with the volume

and backlog of that retained by the SSES CR process.

As noted above, trend

assessment

of individual CR files is performed by the OES evaluators at the initial OES

screening meeting, based on their knowledge of past events.

The licensee

acknowledged that more can be done.

Efforts are being initiated to implement more

structured trending activities (e.g., keyword searching, establishment of indicators, etc.)

11

OES also provides weekly data trending to the technical staff which includes charts

depicting: the backlog of open condition report actions, number of CR actions issued and

completed per month by department, the number of Level 1 and Level 2 E&APs that

have yet to be developed and are overdue, and a "Top Ten List" of corrective actions to

be implemented.

OES also provides a quarterly briefing on adverse trends through

reference to open "trend" CRs and actions being taken to respond to them. There were

approximately.20 open "trend" CRs at the beginning of the inspection.

Audits

The SSES Corrective Action Program is audited annually by PP8L Nuclear Assurance

Services (NAS). The inspectors reviewed results of the most recent NAS assessment

performed in November -December 1998. The NAS assessment

was thorough, critical,

and well founded.

While the NAS assessment

noted improvement in some areas (issue

identification, timeliness for developing Level 1 ESAPs), it did not find measurable

improvement from the 1997 NAS assessment,

and noted that most corrective actions in

response to the prior assessment

were either untimely, incomplete or inadequate.

The,

1998 NAS assessment

summarized its findings into two general areas:

1) that corrective

actions to address adverse conditions are not always effective in preventing repeat

incidents; and 2) corrective actions to address adverse conditions are not always

implemented quickly enough to prevent repeat incidents.

The NAS assessment

highlighted that improvements in timeliness, trending, and oversight are needed in order

to establish control over the corrective action implementation portion of the CR process.

Improvements in these areas willreduce backlog, and reduce repeat occurrences.

The

SSES staff acknowledged that the problems noted in the NAS assessment

have

occurred in the past, and are still occurring, to a lesser degree.

The NAS assessment

findings along with the findings of other external assessments

of

the CR process (e.g., NAS audit and surveillance findings, INPO assessment

findings,

Cooperative Management Audit Program, CMAP, audits, etc.) are documented

in a CR

and entered into the tracking system for further review.

The Susquehanna

Review Committee (SRC), a corporate level safety review committee,

has a CR Review Subcommittee which performs periodic assessments

of the SSES

corrective action program.

The last SRC review, completed in October 1998, looked at

Level 1 and Level 2 reportable CRs that were recommended for approval by the Plant

Operations Review Committee (PORC). A notable concern from this review related to a

June 1998 CR on SRV acoustic monitors, which indicated that a Licensee Event Report

(LER) was written and that no supplement was expected.

The causal analysis for the

CR indicated that a supplement would be written ifthe cause was found to be different

than initiallystated.

The cause was eventually found to be different but no supplemental

LER was written. The inspectors also identified concerns with the corrective action

program's treatment of problems with the SRV acoustic monitors (discussed CR File

Review below).

12

CR File Review

The following items describe the results of the inspectors'eview of information in the CR

database

and specific CR files:

adverse conditions are promptly identified

no significant delays in initial assessment,

initial investigation, and completion of

operability determinations and reportability determinations.

For more recent CRs

(those opened within the past year), these activities are being completed within a

few days, whereas a year or more ago, these activities took a week or more to

complete.

Root cause assessments

for those which require them are thorough.

Investigations and causal analyses for CRs of lesser significance are generally

thorough, but are occasionally too specific to the system, structure or component

in question, and may not sufficiently explore extent of condition and/or generic

implications. This has been noted by OES, NAS, and other external reviews.

Examples noted by the inspectors were several CRs related to measuring and

test equipment (M8TE), in which corrective actions were focused on repair of the

M8TE and not on evaluation of the plant equipment that may have been tested

with the faulty M8TE. Problems with the non-safety-related emergency diesel

generator (EDG) pneumatic control system (discussed below) provide an

example of a system of lesser safety significance ultimately affecting the

operability of a safety-related system.

In response,

OES noted that recent efforts

have been initiated to not make the required actions too prescriptive, so as not to

restrict a responsible manager from developing appropriate closure.

Evaluation and Action Plans (E8APs) are generally established within the times

prescribed in Procedure NDAP-QA-0702. From the specific files reviewed, the

inspectors found seven (7) EBAPs that were established beyond the procedurally

prescribed due date, but extensions were requested

and approved by CAT, as

permitted by the procedure.

corrective action implementation dates do not correlate with the assigned CR

significance level. Action due dates are routinely extended by the assigned

department.

In a large number of cases, process accountability does not appear

evident until the End-of-Cycle due date approaches.

several instances were noted where final CR closure dates were several months

after the completion of the last action. This would appear to be attributable to CR

backlog and OES workload.

OES closeout reviews,-and independent reviews by NAS, INPO and CMAP are

continuing to find instances of incomplete or inadequate action closure.

There

also appears to be a tendency to adjust actions at the end of the process, e.g., by

categorizing issues as no longer necessary,

by changing actions, or by

13

transferring actions to another CR so that an earlier CR can be closed.

While

such adjustments can be expected in certain situations, better control of the

corrective action implementation portion of the CR process would minimize this

effort:

The inspectors found similar instances.

~Exam

las:

CR 96-1504 (9/1 6/96) and CR 96-2012 (10/31/96).

CRs dealt with an unmonitored

release path that was established from the turbine building exhaust system through the

reactor recirculation pump motor-generator (M-G) set ventilation system.

As a result of

an earlier design change, a damper was set to open upon shutdown of the M-G set

ventilation system, creating the release path.

Upon investigation, PP8L determined that

the design change package did not address'the

potential for establishing an unmonitored

release path. Afterthe repeat occurrence (CR 96-2102), a reportability evaluation

determined that, based on surveillance test results, this release path had existed for both

units for approximately 15 total days between July 15, 1996 and October 31, 1996. This

was deemed not to be reportable based on a conclusion that any releases from this

pathway during the times in question would have been within allowable release limits. In

the summary statement for CR 96-2102, PP8L recognized that a principal causal factor

for this repeat occurrence was due to untimely corrective actions for CR 96-1504.

CR 96-1751 (10/3/96) dealt with a half scram due to a nuclear instrumentation

intermediate range monitor (IRM) Channel B upscale trip. The trip was caused by

instrument spiking as a result of the collapsing field of an Agastat relay. Proposed

corrective actions included modifications for both units to filterthe instrument noise

spiking and procedure changes related to IRM ranging.

The Unit 1 instrumentation

modifications were completed in 1998 and the Unit 2 modifications are scheduled for

completion in March 1999. The procedure changes, which were scheduled to be

completed on December 1, 1997, were not implemented.

Instead, a conclusion was

reached on April 1, 1998, 18 months after the occurrence of the half scram, that the

modifications were adequate to reduce the probability of a half scram during startup and

shutdown conditions.

CR 3077 (9/1 7/97) dealt with an audit finding that a prior CR (97-1796) was closed

without performing all required actions, in that work to repair damaged rubber lining

inside a condensate

demineralizer transfer inlet line was not scheduled until after the CR

was closed.

Also, the cause determination was never done to address why the rubber

was coming offthe pipe. The closure mechanism for CR 97-3077 was to change the

classification of the CR from a Level 3 EVAL(requiring evaluation), to a Level 3

CORRECT (only requiring correction), and delete the requirement for engineering to

perform a cause determination review. Since the equipment in question is not safety-

related, the level of response

is at the license's prerogative.

However, the method of

resolution appeared to be a mechanism of convenience to eliminate an assigned action

that had not been accomplished.

14

CR 97-3199 (9/1 7/97) documented the improper closure of two earlier CRs (97-0771

(3/19/97) and 97-0801 (3/22/97)). The earlier CRs identified manganese

deposits on the

inner tube diameters for the core spray pump room coolers and the A and B residual

heat removal (RHR) service water heat exchangers.

The CRs documented an

acceptable cleaning method that was not completed before the CRs were closed.

The

heat exchangers are now scheduled for cleaning in May 1999,'more than two years after

initial identification.

CR 98-2088 (6/1 2/98) dealt with a control rod that was not positioned as required during

a control rod startup sequence.

One of the assigned actions was to form a team to

develop a Reactivity Management Improvement Plan. The CR file indicated that this

action was transferred to another similar CR (98-2267) under which it would be

implemented.

Upon review, CR 98-2267 was not particularly similar to CR 98-2088, i.e.,

it was primarily a maintenance

item with no human performance issues.

The referred

action was not located in CR 98-2267.

The OES Supervisor indicated that, to his

recollection, the Reactivity Management Improvement Plan had been developed and that

he would review it to determine why it was not appropriately captured in the CR process.

CR 87725 (12/30/98) identified four (4) Level 3 CRs that had been closed based on a

fifth CR.

The fifth CRwas closedinfavorofa

"trend" CR. The ESAP ofthe trend CR

did not address the specific issues for the prior CRs. The issues were primarily

administrative items dealing with material traceability, use of procedure forms, and

quality control notification.

Safety relief valve (SRV) acou'stic monitor problems:

Numerous CRs were written in 1998 regarding continuing problems with the SRV

acoustic monitors. While one of these CRs identified that corrective actions were not

preventing failures of the sensor cable connectors, additional problems persisted.

More

recent evaluations, including a containment temperature study, have found that higher

drywell temperatures

near the SRV acoustic monitors have a significant affect on the

expected life of electrical components

in the area.

Allof the SSES Unit 1 SRV acoustic

monitor accelerometers

were replaced in July 1998, and efforts are still on progress to

determine qualified life based on the new containment temperature profiles. While it

appears that this matter may be approaching final resolution, related issues have been

raised in the CR process since the 1994-1995 time frame. Since that time, this matter

has resulted in three Technical Specification required shutdowns and three Notices of

Enforcement Discretion.

It does not appear that the CR process was effective in

'esolving this issue in a timely manner.

Emergency diesel non-safety related pneumatic control system problems:

NRC Inspection Report 50-3878388/99-01

documented recent problems with the "B"

EDG non-safety-related

pneumatic control system.

Briefly, on January 26, 1999, during

operability testing of the "B" EDG, an automatic cooldown run was not competed due to

a failed diaphragm on a pressure switch. The failure of the diaphragm admitted carbon

into the pneumatic control system, causing a subsequent

problem with the cooldown run

15

due to clogging of a check valve. The following day, the "B" EDG was taken out of

service for additional work on the pneumatic control system.

Upon reconnection of the

"E" EDG to place it back into service, it shutdown prior to competing its cooldown run

and was declared inoperable.

The"E" EDG was returned service, tested and declared

operable late on January 28, 12999.

A review of the CR database

found numerous (8) prior CRs related to problems with the

non-safety-related

pneumatic control system.

On January 29, 1999, a "trend" CR was

initiated. However, the events of January 26, 1999, demonstrate that prior corrective

actions were neither effective or timely.

Recent overcurrent protection failures

On January 2, 1999, due to overcurrent protection failure, a normal feeder breaker

tripped, causing automatic startup of several pumps ('A'tator cooling, 'A'lectro-

hydraulic control system pump, standby and emergency lube oil pumps for the reactor

feed pump turbine and seal oil system).

The loads were stripped and the breaker re-

closed.

Some loads were not restored pending an evaluation by electrical maintenance.

CR 87595 was initiated. This was the fifth similar failure in a one month period.

Before

this failure, a "trend" CR (82734) had been written to document the previous four

failures. More accelerated corrective action would appear to have been prudent in this

instance.

c.

Conclusions

The CR process is a high volume, low threshold corrective action system that is

acceptable to meet the requirements of 10 CR 50, Appendix B, Criterion XVI. Adverse

conditions are promptly identified and the process appears to be widely accepted for

use, and is used by a broad cross section of the plant staff. There are no significant

delays in the initial assessment,

investigation, and completion of initial operability and

reportability determinations.

Initial investigations and root cause assessments

for issues

of higher safety significance are thorough.

Investigations and causal analyses for CRs of

lesser safety significance are generally thorough, but there are some instances where

extent of conditions and/or generic implications may not be sufficiently explored.

The CR process is focused on accomplishing initial reviews, reportability and operability

determinations, cause assessments,

and establishment of proposed corrective actions to

correct the condition and prevent recurrence.

However, process accountability is not

readily apparent in the corrective action implementation portion of the process.

Corrective action implementation dates do not correlate with the assigned significance

level. Action due dates are controlled by the responsible manager who may change

them during the course of implementation. The only procedural requirement regarding

corrective action implementation is refueling outage related with the shortest lead time

being approximately 7-10 months, and the longest lead time being approximately 31-37

months.

The minimal administrative control over the corrective action implementation

portion of the process contributes to a high process backlog.

16

Internal reviews by OES and external reviews by NAS, CMAP, INPO, and SRC are

continuing to find incomplete or inadequate corrective action closure. A recent process

change requiring OES to review competed actions to ensure that the actions satisfies the

one prescribed, is reducing the amount of items identified. However, problems persist in

this area.

Annual assessments

of the CR process by NAS were thorough, critical, and well

founded.

Past assessments

(1997 and 1998) have identified most of the concerns noted

above.

V. Mana ementNleetin

s

X1

Exit Meeting Summary

The inspectors discussed the inspection results with members of PP8 L management during the

inspection on January 22 and 29, 1999. A formal inspection exit was conducted

February 19, 1999.

The inspectors asked PP&L whether any materials examined during the inspection should be

considered proprietary.

No proprietary information was identified.

PARTIALLIST OF PERSONNEL

CONTACTED'enns

lvania Power and Li ht

R. Saunders, Vice President of Site Operations

G. Kuczynski, General Manager, SSES

'. Male, Manager of Nuclear Assurance

T. Iorfida, Manager of Special Projects

A. Dominguez, Employee Concerns

R. Wehry, Supervisory Licensing Engineer

M. Golden, Nuclear Systems Engineering Supervisor

J. Maertz, Nuclear Systems Engineering Supervisor

S. Ellis, Licensing Engineer

J. Akus, System Analyst

U.S. Nuclear Re ulato

Commission

S. Hansell, Senior Resident Inspector

J. Richmond, Resident Inspector

A. Blarney, Resident Inspector

17

INSPECTION PROCEDURES USED

Tl 2515/139

Inspection of Licensee's Implementation of Generic Letter 96-01 Testing of

Safety Related Logic Circuits

IP 40500

Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

~Oened

None

ITEMS OPENED, CLOSED, AND DISCUSSED

Closed

None

LIST OF ACRONYMS USED

CAT

CMAP

CR

DCP

ESAP

ECO

ECP

EDG

EHC

FSAR

GL

HPES

IERP

IKM

INPO

IRM

ITS

LDCN

LER

LOCA

LOOP

M8TE

M-G

NAS

NDAP

NIMS

NRC

NRR

Corrective Action Team

Cooperative Management Audit Program

Condition Report

Design Change Package

Evaluation and Action Plan

Engineering Change Order

Employee Concerns Program

Emergency Diesel Generator

Electro-Hydraulic Control System

Final Safety Analysis Report

Generic Letter

Human Performance Evaluation System

Industry Events Review Program

Installation KickoffMeeting

Institute of Nuclear Power Operators

Intermediate Range Monitor

Improved Technical Specification

Licensing Document Change Notice

Licensee Event Report

Loss-of-Coolant Accident

Loss of Offsite Power

Measuring and Test Equipment

Motor Generator

Nuclear Assurance Services

Nuclear Department Administrative Procedure

Nuclear Information Management System

Nuclear Regulatory Commission

Office of Nuclear Reactor Regulation

18

OES

PMP

PORC

PP8L

QA

RHR

SRC

SRV

SSES

Operating Experience Services

Plant Modification Package

Plant Operations Review Committee

Pennsylvania Power and Light

Quality Assurance

Residual Heat Removal

Susquehanna

Review Committee

Safety Relief Valve

Susquehanna

Steam Electric Station

C7

0