ML17164A729
| ML17164A729 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 07/31/1998 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17164A727 | List: |
| References | |
| 50-387-98-03, 50-387-98-3, 50-388-98-03, 50-388-98-3, NUDOCS 9808110121 | |
| Download: ML17164A729 (36) | |
See also: IR 05000387/1998003
Text
US. NUCLEAR REGULATORY COMMISSION
REGION I
Docket Nos:
License Nos:
50-387, 50-388
Report No.
50-387/98-03, 50-388/98-03
Licensee:
Pennsylvania Power and Light Company
2 North Ninth Street
Allentown, Pennsylvania
19101
Facility:
Susquehanna
Steam Electric Station
Location:
P.O. Box 35
Berwick, PA 18603-0035
Dates:
April 28 through June 8, 1998
Inspectors:
K. Jenison, Senior Resident Inspector
J. Richmond, Resident Inspector
A. Lohmeier, Senior Reactor Engineer
T. Burns, Reactor Engineer
Approved by:
Clifford Anderson, Chief
Projects Branch 4
Division of Reactor Projects
'P808iiOi2i 98073K
ADQCK 05000387
6
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EXECUTIVE SUMMARY
Susquehanna
Steam Electric Station (SSES), Units
1 5. 2
NRC Inspection Report 50-387/98-03, 50-388/98-03
This integrated inspection included aspects of Pennsylvania
Power and Light Company's
(PPS.L's) operations and maintenance activities at SSES.
The report covers a 6-week
period of resident inspection as well as a region based inspection.
~Oerations
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Operator activities in support of the Unit 1 shutdown for refueling, the Unit 1 restart
following refueling, and Unit 2 shutdown to repair the 2A recirculation pump were
adequate
and conservative.
(Section 01.1)
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The alignment of eight safety related systems were found to be adequate.
The
licensee conducted plant operations in accordance with SSES procedures,
and
established effective equipment alignment and operability.
(Section 01.2)
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Operators were observed to respond well to a selection of seven alarmed
conditions, including a loss of Residual Heat Removal system cooling and an
infrequently occurring condition (power coast down). Appropriate SSES procedures
were adhered to, operability and impact on plant equipment were controlled, and
actions were adequately performed, communicated and documented.
(Section
01.3)
Operator response to the discovery of a misaligned resin effluent valve was in
accordance with the PPSL
Equipment Status Control Event procedure. Operators
responded well and conservatively.
There was no safety impact associated with
the misaligned component.
(Section 02.1)
A sample of operator log entries was observed to be complete and accurate.
A
specific series of operator log entries accurately reported equipment status tag data,
Technical Specification requirements,
and condition report data.
(Section 02.2)
Twenty seven safety related initial Operability Determinations (ODs) and Condition
Reports (CRs) were reviewed in detail and were found to be'adequately
performed.
Two PPKL OD procedural requirements were not being consistently implemented by
the licensee (consideration of compounded deficiencies and all applicable operating
conditions).
Failure to implement these procedural requirements
has the potential
to affect the quality of ODs, but, no issues of safety significance were identified by
the inspectors in the selected sample.
(Section 04.1)
Maintenance
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Seventeen
of nineteen pre-planned maintenance
activities observed/reviewed
were
found to be appropriately conducted
and controlled; the remaining two maintenance
activities are discussed
in detail in other sections of this report.
Overall,
0
Executive Summary (cont'd)
maintenance
proced ural controls were determined to be general in nature and did
not prescribe some activities performed by maintenance
personnel.
Specifically,
performed activities for which there were no detailed guidance included; emergency
diesel generator
(EDG) valve grinding, valve lapping technique, and valve seat
tightness testing.
Each of these activities were identified by the inspectors
as
potential contributors to a failed EDG performance test.
(Section M1.1)
Two emergency diesel generator
(EDG) maintenance
activities were inadequate,
resulting in a violation of NRC requirements.
Under Work Authorization (WA)
H50056, dated February 6, 1996, maintenance technicians installed repair parts on
the "C" emergency diesel generator
(EDG) that had not received proper quality
receipt inspections and were potentially defective materials.
Under WA H70311,
dated September 26, 1997, maintenance technicians installed a defective EDG head
on the "A" EDG that had not received
a proper quality receipt inspection.
The
defective head caused
a February 3, 1998, EDG performance test abort.
(Section M1 A)
Inservice inspections
(ISI) were performed acceptably, with qualified personnel and
approved procedures.
In general, proper implementation, appropriate examination
documentation,
and adequate
PPRL oversight were observed.
The ISI were
thorough and of sufficient extent to determine the integrity of the components.
Non-
conforming conditions were adequately identified and reported for disposition.
However, two instances of work package problems were identified by the NRC,
including an outdated procedure
and an inaccurate qualification record, which
constituted
a violation of NRC document control requirements of minor safety
significance.
(Section M2.1)
Also, symptomatic of problems in work planning, on at least three occasions,
scheduled
NDE work was delayed from hours to a day due to various work planning
problems.
While these delays of themselves did not represent
a regulatory concern,
the high frequency of delays did appear to be related to weak work planning, which
could potentially affect the quality of NDE work, including As-Low-As-Reasonably-
Achievable (ALARA). (Section M2.1)
TABLE OF CONTENTS
EXECUTIVE SUMMARY
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Summary of Plant Status
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I. Operations
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Conduct of Operations ...
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01.1
Operator Shift Activities
01.2
Operational Safety System Alignment
01.3
Operator's Response to Alarmed, Unexpected and Infrequently
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Performed Situations
01.4
Equipment Status Tags
Operational Status of Facilities and Equipment
02.1
Equipment Status Control Event - Valve Misalignment
02.2
Operator Logs
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04.1
Operability Determinations and Condition Report Action Items
Miscellaneous Operations, Issues
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II. Maintenance
M1
Conduct of Maintenance........ ~....... ~.......
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M1.1
Pre-Planned
Maintenance ActivityReview.
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M1.2
Surveillance Test ActivitySample Reviews
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M1.3
Radiological Waste Supply Filter Replacement
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M1.4
Repair of the "A" and "C" Emergency Diesel Generators
M2
Maintenance and Material Condition'of Facilities and Equipment
M2.1
Inservice Inspection Program..........
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V. Management Meetings....
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Exit Meeting Summary ..
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ATTACHMENT
Attachment
1 - Inspection Procedures
Used
- Items Opened, Closedand Discussed
- List of Acronyms Used
0
Re ort Details
Summer
of Plant Status
Susquehanna
Steam Electric Station (SSES) Unit 1 commenced
a power coast down,
plant shutdown, and a refueling and inspection outage prior to this inspection period.
On
June 5, 1998, Unit 1 began
a normal reactor startup from its 10th refueling and inspection
outage and continued throughout this inspection report period at 100% power.
Unit 2 operated at 100% during the inspection period, except for a forced outage, to
perform repairs on the 2A reactor recirculation pump seal, which began on June 6, 1998.
I. 0 erations
01
Conduct of Operations
'1.1
0 erator Shift Activities
a.
Ins ection Sco
e 71707
r
Routine activities of plant control operators
(PCOs), nuclear plant operators
(NPOs)
and unit supervisors
(USs) were observed throughout the inspection period.
b.
Observations
and Findin s
Routine operator activities were prescribed, concisely communicated,
and performed
in accordance with SSES operations department procedures.
Shift turnovers were
observed to be detailed and complete.
Operator activities in support of the Unit 1 refueling and inspection outage, the
Unit 1 restart following refueling, and Unit 2 shutdown to repair the 2A recirculation
pump were adequate
and conservative.
The inspectors discussed
plant conditions. with oncoming PCOs and USs following
shift turnovers and observed that sufficient information and status were transferred
to the oncoming shift to ensure the safe'operation of the units.
C.
Conclusions
Operator activities in support of the Unit 1 shutdown for refueling, the Unit 1 restart
following refueling, and Unit 2 shutdown to repair the 2A recirculation pump were
adequate
and conservative.
'Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized reactor inspection report outline.
Individual reports are not expected to address
all outline topics.
1
2
01
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0 erational Safet
S stem Ali nment
a.
Ins ection Sco
e 71707
The inspectors observed plant operation to verify that the facility was operated
safely and in accordance with procedures
and regulatory requirements.
Inspectors
observed the control room alignment of selected safety related systems.
b.
Observations
and Findin s
The inspectors observed that the licensee conducted plant operations in accordance
with procedures,
and effective controls were implemented for safe plant operation.
Overall equipment operability, material condition, and housekeeping
conditions were
good.-
The alignment/operability of eight selected safety related systems including,
engineered safety features and on-site power sources were verified. Verification of
the functioning of a refueling heat sink (supplemental decay heat removal system)
was performed in the field and the control room.
The inspectors identified several minor housekeeping
and material condition items,
that did not affect system operability, and communicated the items to the licensee
for its review.
c.
Conclusions
The alignment of eight safety related systems were found to be adequate.
The
licensee conducted plant operations in accordance with SSES procedures,
and
established effective equipment alignment and operability.
01.3
0 erator's Res
onse to Alarmed
Unex ected and lnfre uentl
Performed Situations
a.
Ins ection Sco
e 71707
During control room observations, the inspectors observed/reviewed
PCO and US
response to alarmed, unexpected,
and infrequently performed situations to
determine compliance with Technical Specification (TS) and SSES operating
procedures.
b.
Observations
and Findin s
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Operator responses
to the seven alarmed conditions were observed to be aggressive
and in accordance with TSs and SSES operating procedures.
The control room staff
responded well to a loss of Residual Heat Removal system cooling to Unit 1.
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c.
Conclusions
Operators were observed to respond well to a selection of seven alarmed
conditions, including a loss of Residual Heat Removal system cooling and an
infrequently occurring condition (power coast down). Appropriate SSES procedures
were adhered to, operability and impact on plant equipment were controlled, and
actions were adequately performed, communicated and documented.
01.4
E ui ment Status Ta s 71707
The inspectors reviewed four equipment status tags that were in effect and/or being
applied to plant systems.
It was observed that the status tags were properly
prepared and authorized.
Some of the tags required supplemental
NRC review of
additional materials, to determine if the systems were still capable of performing as
designed; no violations of NRC requirements were identified.
02
Operational Status of Facilities and Equipment
02.1
E ui ment Status Control Event - Valve Misali nment
a.
Ins ection Sco
e 71707
The inspectors observed/reviewed
Shift Supervisor (SS), US, and Auxiliary System
Operator (ASO) response to a licensee identified misalignment of a Unit 1 resin tank
effluent line drain valve, which occurred during a Unit 1 reactor coolant system
hydraulic pressure test.
b.
Observations
and Findin s
Operator response, to the discovery of a valve misalignment, was in accordance
with the Equipment Status Control Event procedure, NDAP-QA-302. The system
was realigned and a condition report (CR) was initiated to determine root cause.
The inspectors observed the licensee responded to the misalignment conservatively
and in accordance with established
SSES procedures.
There was no safety impact
associated with this specific misaligned system.
c.
Conclusions
Operator response to the discovery of a misaligned resin effluent valve was in
accordance with the PP5L
Equipment Status Control Event procedure. Operators
responded well and conservatively.
There was no safety impact associated with
the misaligned component.
a.
Ins ection Sco
e 71707
During routine control room tours, the inspectors made detailed reviews of PCO,
US, Limiting Condition for Operations (LCO), BypassWork Around, and Equipment
Status logs.
b.
Observations
and Findin s
Overall, operator logs were observed to adequately document and discuss plant
conditions and events.
The inspectors questioned the completeness
of some log
entries, the age and necessity of some work arounds, status controlled plant
conditions, and bypasses,
but no safety impacts or violations of NRC requirements
were identified.
c.
Conclusions
A sample of operator log entries was observed to be complete and accurate.
A
specific series of operator log entries accurately reported equipment status tag data,
Technical Specification requirements,
and condition report data.
04
Operator Knowledge and Performance
04.1
0 erabilit
Determinations and Condition Re ort Action Items
a.
Ins ection Sco
e 71707
The inspectors reviewed a sample of Operability Determinations (ODs) and
Condition Report (CR) action items to determine if degraded conditions were
identified, were initiallyresolved with conservatism,
and long term corrective
actions were completed.
b.
Observations
and Findin s
Twenty seven CR corrective actions were reviewed.
Each of the CRs contained an
operability determination (OD).
In general, the ODs were found to have been
adequately performed.
The inspectors questioned the adequacy of one OD and had
two general findings with potential for significance.
The OD and two general
findings are discussed
below:
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OD for CR 98-1328, "C" Emergency Diesel Generator
(EDG) Air Start Valves
This OD was written in response to NRC concerns that repair parts (air start valve
components) were installed on the "C" EDG without a proper receipt inspection,
adequate control over the maintenance
installation activities or a detailed operability
determination.
The repair parts that did not receive proper receipt inspection and
control included components such as air start valves, valve springs, slide valves,
retaining devices, slide valve rings and valve seats.
The initial OD was limited to one component failure mode (failure of one air start
valve to open) and concluded that the "C" EDG was operable,
The OD concluded
in-head air start valves were provided in sufficient redundancy to ensure that the
EDG would start within acceptable
limits, and that the installation of these
components would not impact the ability of the EDG to start or accelerate.
The OD
analysis for the one failure mode was based upon operating experience related to a
stuck shut air start valve, system design features, test, results related to the failure
of air start valves to open on the "C" EDG, engineering judgement and a vendor
letter. The inspectors reviewed this initial OD and determined that for one
component failure mode (failed shut air start valve) the licensee analysis was
adequate.
However, the licensee did not address other failure modes of the potentially
defective components.
One component failure mode (failed open air start valve)
occurred on the "A" EDG just prior to the writing of the OD (see section M1.4 of
this report)
~ The inspectors determined that the initial OD did not address the ability
of the EDG to withstand a failed open air start valve, or other potential failures (ex.
FME from broken slide valve rings).
In addition, neither the vendor letter nor the
initial OD addressed
the ability of the "C" EDG to startup, load and run long term
with multiple potentially defective parts installed.
Subsequent to the
inspectors'uestions,
the licensee revised its initial OD.
The revised OD considered the impact defective parts could have on "C" EDG
operability and determined that the EDG was currently operable.
The revised OD
satisfactorily established that part failure was not expected based on the premise
that the EDG had successfully started and run approximately 50 times since the
application of the parts in question.
During these tests,
EDG performance was
adequate
including several run times of moderate length.
The inspector reviewed the revised OD and concluded that 50 successful starts
were statistically significant, and an indication that the component failure modes in
addition to a failed shut air start valve were not likely to occur in the future.
The
inspector determined that the revised OD was adequate
and that the "C" EDG was
General Finding 1, Compounding of Deficiency Conditions
NDAP-QA-703, section 5.2, indicated that ODs consider compounded conditions,
where each condition by itself may not result in a system structure or component
(SSC) in-operability but when taken together, may result in SSC in-operability.
In
addition, the procedure states that system interrelationships should be considered.
Section 6.3 of NDAP-QA-703 requires the consideration
be documented.
In the sample of CR ODs reviewed, the inspectors identified no instances where this
required action was performed and documented or was determined to not be
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applicable and documented.
Example:
In the case of the "C" EDG discussed
above, there were several outstanding WAs, performance test findings and CR
action items against "C" EDG when the CR OD was written. There was no
indication whether the review for compounded condition was applicable or was
performed.
With respect to the sample of CR ODs reviewed during this inspection,
no instances of compounded conditions affecting safety related equipment
operability were identified.
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General Finding 2, Operating Conditions
NDAP-QA-703, section 6.2, indicated that ODs evaluate the degraded condition for
impact on the component's function for all operating conditions.
Section 6.3 of
NDAP-QA-703 requires the evaluation be documented.
Based on the sample of CR ODs reviewed, the inspectors identified that some CR
ODs for safety related equipment did not document an evaluation of degraded
conditions for all applicable operating conditions, but focused on some mitigating
alignment or unit operating condition. With respect to the sample of CR ODs
reviewed during this inspection, no instances were identified where the failure to
consider all operating conditions affected the safe operation of the units.
C.
Conclusions
Twenty seven safety related initial Operability Determinations (ODs) and Condition
Reports (CRs) were reviewed in detail and were found to be adequately performed.
Two PPS.L OD procedural requirements were not being consistently implemented by
the licensee (consideration of compounded deficiencies and all applicable operating
conditions).
Failure to implement these procedural requirements
has the
potential
to affect the quality of ODs, but, no issues of safety significance were identified by
the inspectors
in the selected sample.
08
Miscellaneous Operations Issues
08.1
Licensee Event Re ort Review (92700)
Closed
LER 50-387 97-016
Fire Protection Surveillance Not Completed Within Time Required by Technical
Specifications
The licensee determined through an audit of the fire protection program that
monthly TS 4.7.6.5 surveillance requirements were not met.
The root cause of the.
failure to meet TS requirements was determined by the licensee to be the use of a
scheduling tool that incorporated
a fixed date for each surveillance instead of
calculating the start date from when the surveillance was last performed.
The inspectors evaluated (through direct inspection, interviews and observation) the
long term effect of the licensee's corrective actions, which included changes to the
scheduling method used by the licensee.
No instances were identified where
missed surveillance periods resulted in significant degraded equipment conditions.
The inspectors determined that the root cause of the missed surveillance was
inadequate control over work planning and scheduling of TS required activities.
A sample of other surveillance were performed and with the exception of response
time testing (see IR 50-387,388/97-03)no
other examples were identified. The
failure=to test fire system related equipment. in accordance with the schedule set by
TS had little safety impact.
This licensee identified and corrected event was treated
as a non-cited violation, consistent with Section VII.B.1 of the NRC Enforcement
Policy in NRC IR 50-387,388/97-07.
This LER is closed.
Closed
LER 50-387 97-017
Mis-positioned "A" Emergency Diesel Generator Governor Knob
On July 11,'1997, the NRC resident inspector identified a mis-positioned "A"
Emergency Diesel Generator (EDG) governor load control knob.
The mis-positioning
event, escalated
enforcement and the licensee's corrective actions were addressed
in NRC Ins'pection Report 50-387,388/97-06.
Based on direct inspection,
interviews and observation of the issues discussed
in this LER, the inspector
determined that the licensee adequately reported the mis-positioned component.
Other aspects of the issues identified in the LER are addressed
in NRC escalated
enforcement as discussed
in NRC Inspection Report 50-387,388/97-06.
This LER is
closed.
Closed
LER 50-387 97-008-00
Instrument Response
Time Testing
On March 26, 1997, with Unit 1 at 100% power and Unit 2 in refueling, PPSL
determined that the requirements of TS surveillances 4.3.1, 4.3.2, and 4.3.3 for
Response Time Testing were not fulfilled. In NRC IR 50-387,388/97-03,
the NRC
dispositioned
LER 50-387/97-008concerning
the identification that Technical
Specification Response
Time Testing requirements were not being met. A sample of
other surveillances was performed (using direct inspection, interviews and
observation of the issues)
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In reviewing this matter at other sites where it has not been dispositioned, the NRC
concluded that the PPRL LER was insufficient in that it did not address
an
inadequate
10 CFR 50.59 safety evaluation as a cause of not meeting the TS
requirements
and therefore did not specify any corrective actions proposed or taken
for the inadequate safety evaluation.
While the NRC is not reopening any
enforcement action pursuant to Section XIII of the NRC's Enforcement Policy, the
licensee
is requested to either supplement the LER or otherwise address
on the
docket SSES corrective actions taken or proposed for the failure of your 10 CFR 50.59 process to identify that the elimination of Response
Time Testing
requirements from the FSAR required a TS amendment.
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Closed
LER 50-387 97-018
Relay Logic Not Response Time Tested
On August 7, 1997, the licensee identified that specific relays related to two Unit-1
reactor building closed cooling water isolation valves had not been included in its
original response time testing program.
The appropriate tests were subsequently
completed acceptably.
The inspectors reviewed the licensee's corrective actions
(employing direct inspection, interviews and observation of the issues discussed
in
this LER) and determined that the identification of the untested relays was the result
of corrective actions for an violation identified in Inspection Report 50-387,388/97-
03. The subject violation addressed
the failure to perform TS testing.
The root
cause for this event was different that the root cause for the violation identified in
Inspection Report 50-387,388/97-03.
Therefore, this licensee identified and
corrected event was treated as a non-cited violation, consistent with Section VII.B.1
of the NRC Enforcement Policy. This LER is closed.
(NCV 50-387/98-03-01)
Closed
LER 50-387 97.-023
Fire Protection Surveillance Requirements Not Included In the Susquehanna
Surveillance Program
The license determined through an audit of the fire protection program that TS 4.7.6.3 surveillance requirements were not included in the SSES surveillance
program.
The root cause of the failure to meet TS requirements was determined by
the licensee to be the inadequate control of fire protection modification and
licensing processes.
The errors occurred between 1988 and 1991, and the
inspector verified that the present SSES controls, if properly implemented, would
have prevented the errors that occurred in the past.
The inspector reviewed the
licensee's corrective actions that included equipment testing, procedure changes
and training, and determined that the licensee's corrective actions were adequate.
No instances were identified where missed surveillances were followed by
significant degraded equipment conditions.
A sample of other surveillance was performed (using direct inspection, interviews
and observation of the issues) and with the exception of response time testing (see
IR 50-387,388/97-03)no
other examples of missed surveillances were identified.
The failure to test fire system equipment (seventeen
doors, carbon dioxide
suppression
equipment, detection equipment and one damper) in accordance with
the TS had little safety impact because
when tested, the equipment performed
appropriately.
Therefore, this licensee identified and corrected event was treated as
a non-cited violation, consistent with Section VII.B.1 of the NRC Enforcement
Policy. This LER is closed.
(NCV 50-387,388/98-03-02)
Closed
LER 50-387 96-015
4.16 KV Breakers Not in Dynamically Qualified Position
PPSL identified that Class-1E 4.16KV switchgear for both units were dynamically
qualified with breakers
in the racked in position only. With breakers in either the
racked out and installed in the cubicle position or the racked into 'test'osition, the
4.16KV switchgear would not be dynamically qualified due to inadequate
restraint
of the breaker in those positions.
PP&L determined, based on the breaker
alignment, that seven breakers were, at various times, in positions other than the
dynamically qualified position, which affected three out of four 4.16KV switchgear
busses
per unit.
Technical Specification 3.8.3.1 requires four load group channels of 4.16KV
switchgear to be operable with the reactor in Operation Condition 1, 2, and 3.
Since the seven breakers were in positions other than the dynamically qualified
position, three of the four 4.16KV switchgear busses
per unit were inoperable from
the time of each units's original startup until compensatory measures
were
implemented on November 5, 1996.
Failure to have the required operable load
group channels of 4.16KV switchgear is a violation of Technical Specification 3.8.3.1
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PP&L placed the switchgear in an analyzed configuration after the condition was
identified.
PP&L designed and installed modifications to secure open switchgear
cubicle doors and established
administrative controls for the position of breakers in
switchgear cubicles.
The inspectors concluded that the PP&L corrective actions
addressed
the violation.
The inspectors noted that excellent questioning attitude by PP&L led to
identification of the design deficiency, and ultimately resulted in issuance of NRC
Information Notice 97-53, Circuit Breakers Left Racked Out in Non-Seismically
Qualified Positions.
The issue also was not likely to be identified by routine PP&L
activities.
The corrective actions were comprehensive
and performed within a
reasonable time frame,
In accordance with Section VII.B.3 of the Enforcement
Policy, the NRC is exercising enforcement discretion and not citing the Technical specification 3.8.3.1 violation. This LER is closed.
(NCV 50-387/98-03-03)
II. Maintenance
Conduct of Maintenance
Pre-Planned
Maintenance Activit Review
Ins ection Sco
e 62707
The inspectors observed/reviewed
selected portions of pre-planned maintenance
activities, to determine whether the activities were conducted in accordance with
NRC requirements
and SSES procedures.
Observations
and Findin
s
Maintenance activities authorized by nineteen WAs were observed/reviewed
during
this inspection and seventeen
were found to be adequately performed.
In addition,
selected personnel qualifications, equipment permits (e.g., tagouts), procedures,
10
drawings, and/or vendor technical manuals associated with the maintenance
activities were also reviewed and found to be acceptable.
In general, maintenance
personnel were knowledgeable of their assigned activities.
Field supervision was
present for the observed activities.
The procedural guidance was general in nature
with references
identified to obtain detailed information.
Of the nineteen WAs, the inspector determined two WAs entailed inadequate
maintenance activities.
The two WA activities are discussed
in section M1.4
(H50056 and H70311) of this report. Seventeen
of nineteen pre-planned
maintenance activities observed/reviewed
were found to be appropriately conducted
and controlled.
Overall, maintenance
procedural controls were determined to be
general in nature and did not prescribe some activities performed by maintenance
personnel
~ Specifically, performed activities for which there were no detailed
guidance included; emergency diesel generator valve grinding, valve lapping
technique, and valve seat tightness testing.
Each of these activities were identified
by the inspectors as potential contributors to a failed emergency diesel generator
performance test.
Conclusions
Seventeen of nineteen pre-planned maintenance activities observed/reviewed
were
found to be appropriately conducted and controlled; the remaining two maintenance
activities are discussed
in detail in other sections of this report.
Maintenance
procedural controls were determined to be general in nature and did not prescribe
some activities performed by maintenance
personnel.
Specifically, performed
activities for which there were no detailed guidance included; emergency diesel
generator
(EDG) valve grinding, valve lapping technique, and valve seat tightness
testing.
Each of these activities were identified by the inspectors as potential
contributors to a failed EDG performance test.
Surveillance Test Activit Sam
le Reviews (61726)
The inspectors observed/reviewed
selected portions of seven surveillance activities.
The observed/reviewed
surveillance activities were determined to conform to the
requirements of TS and met PP&L administrative requirements (i.e., approvals,
personnel qualifications, scheduling, and permits).
Components were properly
removed from service and, when appropriate, the TS LCOs were documented
and
met.
The surveillance activities were determined to have been accomplished by
qualified and trained personnel.
No violations of NRC requirements were identified.
Radiolo ical Waste Su
I
Filter Re lacement
(62707)
Maintenance activities authorized by WAs P71811, S71372, and S72260 were
reviewed, specifically to evaluate the job task certification of assigned maintenance
personnel.
The maintenance
activities that were reviewed were performed by
mechanical, electrical, and instrument maintenance technicians.
For those activities
requiring specific certification, safety related activities, and activities identified by
11
detailed descriptions
in the WAs, the inspectors concluded that the technicians
were adequately trained and certified.
In one non safety related activity, a temporary differential pressure measurement
device, dwyer manometer, was applied around an installed non-safety related
instrument.
The temporary differential pressure
measurement
device was applied by
. electricians, who did not possess
required specific certification to install the
equipment.
A permit was r'equired by licensee procedures but was not applied.
Because there was no impact on the equipment, subsequent
functional tests of the
installed differential measurement
devices were acceptable,
the equipment was not
safety related and the actions taken were reviewed and approved by qualified first
line supervisors representing
all three crafts, there was no violation of NRC
requirements.
As part of the inspection of WA P71811, the inspector reviewed a sample of the
task certification and training records for mechanical, electrical and instrument
maintenance technicians and maintenance first line supervisors.
The inspector
concluded that for safety related activities, the task certification and training
processes
were accredited, met current industry standards
and were adequately
implemented.
M1.4
Re air of the "A" and "C" Emer enc
Diesel Generators
Ins ection Sco
e 62707
The inspectors observed/reviewed
selected portions of pre-planned emergency
diesel generator
(EDG) maintenance activities, and corrective EDG maintenance to
determine whether the activities were conducted in accordance with NRC
requirements
and SSES procedures.
Following a February 3, 1998, emergency diesel generator (EDG) maintenance test
abort, the inspectors reviewed; the licensee's corrective actions for the test abort,
the corrective maintenance activities following the test abort, and the root cause of
the test abort (note: the root cause of the 1998 test abort was related to a previous
1996 failure to adequately control EDG maintenance
activities).
Observations
and Findin s
EDG maintenance
activities were determined to have resulted in two examples of a
violation regarding receipt control inspections of quality material
~
1998 Maintenance Test Abort - "A" EDG Re airs - WA H70311
On September 26, 1997, Work Authorization (WA) H70311 was established to
perform routine maintenance activities on the "A" EDG. Following completion of
these maintenance activities, the "A" EDG underwent
a maintenance test on
February 3, 1998. After approximately 40 minutes of operation at low load (800
kW) nuclear plant operators
(NPOs) noticed indications of overheating on the air
12
start manifold adjacent to the "8L" cylinder. The test was aborted and the EDG
was manually shutdown from the local panel.
The licensee removed the head near the overheated
air start manifold and
determined that the air start valve had stuck in the open position.
The licensee
initiated an Event Review Team (ERT), a root cause evaluation, and Condition
Report 98-0351
~ The inspectors attended one of the ERT working meetings and
reviewed the licensee's root cause activities,
The licensee's activities were
determined to be detailed and conservative with respect to the physical
determination of the failure and the implementation of corrective maintenance.
The aborted maintenance test was caused by a defective EDG head returned from
the PPRL vendor (Cooper).
The EDG head was defective since foreign material was
contained in the repaired EDG head.
The foreign material was not identified in the
PPS.L receipt inspection process.
10 CFR 50, Appendix B, Criterion Vill, Identification and Control of Materials, Parts
and Components,
in part, required that measures
shall be established for the
identification and control of parts and components.
These measures
shall be
designed to prevent the use of incorrect or defective material, parts, and
components.
PPKL procedure, NDAP-QA-0201, Material Control Activities, established the
requirements for receipt inspection for quality materials, and stated that all quality
materials shall be forwarded to the receipt inspection group for inspection in
accordance with procedure NP-QA-0401, Receiving Inspection.
NP-QA-0401,
section 6.1, required', in part, visual inspections for physical damage and
cleanliness.
On September 26, 1997, Work Authorization (WA) H70311 was established to
perform routine maintenance activities on the "A" EDG. The maintenance
activities
installed a defective EDG head that was not receipt inspected
in accordance with
NP-QA-0401, in that the head was not clean and the receipt inspection was not
adequate to identify the foreign material in the,EDG head.
The foreign material
resulted in the defective EDG head which subsequently
caused
an aborted EDG
performance test.
The failure to perform an adequate receipt inspection is example
(a) of a violation of NRC requirements.
(VIO 50-387,388/98-03-04(a))
As part of the inspectors'eview of the 1998 event, a 1996 EDG maintenance
activity was identified which also involved inadequate receipt inspection of safety
related repair parts.
1996 Maintenance Activit - "C" EDG Re
air Parts Recei t Control - WA H50056
On February 6, 1996, WA H50056 was established to perform maintenance
activities on the "C" EDG.
Maintenance technicians installed repair parts that had
not received proper quality receipt inspections.
These repair parts were potentially
defective material.
13
The inspectors identified that on March 5, 1996, a PPSL vendor (Cooper) returned
to the licensee certain air start valves and associated
components,
under service
order 5-54297-5.
The vendor provided documentation stating that they had not
treated these components
as quality materials.
About half of the components were
determined to be damaged and/or otherwise rejected by maintenance technicians
repairing the "C" EDG. However, the other half of the components were installed
on the "C" EDG without receiving receipt inspection from the receipt inspection
group.
10 CFR 50, Appendix B, Criterion Vill, Identification and Control of Materials, Parts
and components,
requires, in part, that measures
shall be established for the
identification and control of parts and components.
These measures
shall assure
that identification of the item is maintained by an appropriate means, either on the
item or on records traceable to the item. These identification and control measures
shall be designed to prevent the use of incorrect or defective material, parts, and
components.
PP&L procedure, NDAP-QA-0201, Material Control Activities, established the
requirements for receipt inspection for quality materials, and stated that all quality
materials shall be forwarded to the receipt inspection group for inspection in
accordance with procedure NP-QA-0401, Receiving Inspection.
NP-QA-0401,
section 6.1, required, in part, item inspections to assure that; item identification and
markings were in accordance with procurement document requirements; applicable
codes and standards were met and vendor specifications were met.
Although the vendor provided documentation with the repair parts stating that they
had not treated the components
as quality materials, the returned parts were
received by SSES maintenance
personnel and were installed into safety related
equipment ("C" EDG) without the receipt inspection group performing the required
receipt inspection.
The failure to perform the required receipt inspections prior to,
installing the safety related repair parts in,the "C" EDG is example (b) of a violation
of NRC requirements.
(VIO 50-387,388/98-03-04(b))
Conclusions
Two emergency diesel generator
(EDG) maintenance
activities were inadequate,
resulting in a violation of NRC requirements.
Under Work Authorization (WA)
H50056, dated February 6, 1996, maintenance technicians installed repair parts on
the "C" emergency diesel generator
(EDG) that had not received proper quality
receipt inspections and were potentially defective materials.
Under WA H70311,
dated September 26, 1997, maintenance technicians installed a defective EDG head
on the "A" EDG that had not received
a proper quality receipt inspection.
The
defective head caused
a February 3, 1998, EDG performance test abort.
M2
Maintenance and Material Condition of Facilities and Equipment
M2.1
Inservice lns ection Pro ram
a.
Ins ection Sco
e 73753
The inspector reviewed plans and schedules for the current inservice inspection (ISI)
interval (first outage, second interval, second period) to verify compliance with the
requirements of ASME Section XI and 10 CFR 50.55a(g).
Specific areas inspected
included ASME Section XI ISI program coverage, qualifications and certifications of
the non destructive examination (NDE) personnel,
and
examination results.
In addition, the inspectors observed selected
NDE activities,
including ultrasonic test (UT) of two main steam line welds and one reactor vessel
head spray line weld, liquid penetrant test (LP) of one head spray weld and
magnetic particle test (MT) of two main steam welds.
b.
Observations
and Findin s
NDE contractors performed ISI examinations and PPSL provided oversight which
involved review and approval of qualifications and procedures,
and monitoring of
selected tests.
The inspector found the ISI work activities to be performed
acceptably.
The'ISI ultrasonic, liquid penetrant and magnetic particle test
procedures were approved by both the ISI contractor and PPRL, and were
determined by the inspectors'to
be in accordance with the ASME Code
requirements.
The inspectors found the inspection implementation consistent with the approved
procedures.
The personnel qualification records for six NDE inspectors were
examined and found to be in compliance with the ASME code requirements.
Based
on selected
NRC inspections of two head spray welds, PP&L oversight of contractor
NDE activities was found to be adequate.
During the inspection of qualification records, the quality of work packages
was
also inspected by NRC. The inspector identified two instances
in which the quality
of work packages
was inadequate
and the requirements of 10 CFR 50, Appendix B,
Criterion Vl were not met.
In one case,
an ISI Level II examiner was prepared to perform the magnetic
particle test of welds VNBB211-20-Land VNBB211-20-Pin the main steam
system, using an outdated revision (revision-9) of PPRL procedure NMTWD-
1.
In response to the NRC identifying this issue, licensee personnel obtained
the correct revision of the procedure (revision-10)
~ The out of date
procedure was not used to perform safety related work.
In the second case, the inspector noted errors in the certification
documentation for a Level II ultrasonic examiner.
Performance
Demonstration Initiative (PDI) certificate 332 issued by the Electric Power
15
Research Institute (EPRI), which attested to the qualification of the examiner
in the use of Generic Procedure for the Ultrasonic Examination of Ferritic Pipe
Welds, PDI-UT-1, Revision B, Addenda 0, was found to have errors regarding
the demonstrated
ranges of diameter and thickness.
The documentation had
been issued by EPRI, reviewed and accepted
by the contractor,'and
accepted
by PPSL.
The acceptance
of such errors by PPSL indicated an inadequate
review of contractor qualification records.
These issues constitute
a violation of minor significance and is not subject to formal
enforcement action.
Also, symptomatic of problems in work planning, the inspector noted that on at
least three occasions,
scheduled
NDE work was delayed from hours to a day due to
various work planning problems.
While these delays of themselves
did not
represent
a regulatory concern, the high frequency of delays did appear to be
related to weak work planning, which could potentially affect the quality of NDE
work, including As-Low-As-Reasonably-Achievable
(ALARA)~
Examination data and documentation were reviewed and found to be in accordance
with the ISI procedures
and ASME Code requirements.
NDE personnel performing
inspections had properly identified and recorded indications and, where applicable,
had processed
and re-examined those indications evaluated
as non-relevant.
Non-
conforming conditions were identified, explored for relevance,
and reported on PPS,L
ISI Notification Form 98-010. A Condition Report was initiated as a result of one
non-conforming condition. The tracking of ISI examination results indicated that the
ISI program was in compliance with the ASME Code,Section XI for the specified
penod.
Conclusions
Inservice inspections
(ISI) were performed acceptably, with qualified personnel and
approved procedures.
In general, proper implementation, appropriate examination
documentation,
and adequate
PP&L oversight were observed.
The ISI were
thorough and of sufficient extent to determine the integrity of the components.
Non-
conforming conditions were adequately identified and reported for disposition.
However, two instances of work package problems were identified by the NRC,
including an outdated procedure and an inaccurate qualification record, which
constituted
a violation of NRC document control requirements of minor safety
significance.
Also, symptomatic of problems in work planning, on at least three. occasions,
scheduled
NDE work was delayed from hours to a day due,to various work planning
problems.
While these delays of themselves
did not represent
a regulatory concern,
the high frequency of delays did appear to be related to weak work planning, which
could potentially affect the quality of NDE work, including As-Low-As-Reasonably-
Achievable (ALARA).
0
0
16
V. Mana ement Meetin
s
X1
Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management
at an exit meeting on June 9, 1998.
The licensee acknowledged the findings
presented.
The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary.
No proprietary information was
identified.
ATTACHMENT1
INSPECTION PROCEDURES USED
IP 61726
IP 71707
IP 92700
Onsite Engineering Observations
Surveillance Observations
Maintenance Observations
Plant Operations
Inservice Inspection
On Site Followup of Reports
ITEMS OPENED, CLOSED, and DISCUSSED
~Oened
50-387,388/98-03-04
"A" 5. "C" Emergency Diesel Generator Repairs
(section M1.4)
Closed
50-387,388/98-03-02
50-387/98-03-03
Fire Protection Surveillance Requirements Not Included
In the Susquehanna
Surveillance Program (section'08.1)
4.16 KV Breakers Not in Dynamically Qualified Position
(section 08.1)
, 50-387/98-03-01
50-387/96-01 5
50-387/97-01 6
50-387/97-01 7
50-387/97-01 8
50-387/97-023
Relay Logic Not Response
Time Tested (section 08.1)
LER
4.16 KV Breakers Not in Dynamically Qualified Position
(section 08.1)
LER
Fire Protection Surveiltances Not Completed Within
Time Required by Technical Specifications (section
08.1)
LER
Mis-positioned "A" Emergency Diesel Generator
Governor Knob (section 08.1)
LER
Relay Logic Not Response
Time Tested (section 08.1)
LER
Fire Protection Surveillance Requirements Not Included
In the Susquehanna
Surveillance Program (section 08.1)
Attachment
1
LIST OF ACRONYMS USED
CFR
CR
ERT
IR
KV
kw
LCO
LER
NDAP
NRC
NSAG
NSE
PCO
psIg
SDHR
SR
TS
US
WA
As-Low-As-Reasonably-Achievable
American Society of Mechanical Engineers
AuxiliarySystems Operator
Code of Federal Regulations
Condition Report
Escalated
Enforcement Item
Electric Power Research Institute
Event Review Team
Final Safety Analysis Report
High Pressure
Coolant Injection
[NRC] Inspection Report
Inservice Inspection
Kilovolts
Kilowatts
Limiting Condition for Operation
Licensee Event Report
Liquid Penetrant Test
Magnetic Particle Test
Non-Cited Violation
Nuclear Department Administrative Procedure
Nuclear Plant Operator
Nuclear Regulatory Commission
Nuclear Safety Assessment
Group
Nuclear System Engineering
Plant Control Operator
Performance Demonstration Initiative
Plant Operations Review Committee
pounds per square inch gauge
Quality Assurance
Supplemental Decay Heat Removal
Standby Liquid Control System
surveillance Requirement
Shift Supervisor
Susquehanna
Steam Electric Station
Technical Specification
[NRC] Unresolved Item
Unit Supervisor
Ultrasonic Test
Violation
Work Authorization