ML17164A902

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Insp Repts 50-387/98-05 & 50-388/98-05 on 980914-1002. Violations Noted.Major Areas Inspected:Engineering
ML17164A902
Person / Time
Site: Susquehanna  
Issue date: 11/13/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17164A900 List:
References
50-387-98-05, 50-387-98-5, 50-388-98-05, 50-388-98-5, NUDOCS 9811240054
Download: ML17164A902 (36)


See also: IR 05000387/1998005

Text

U.S. NUCLEAR REGULATORYCOMMISSION

REGION I

Docket Nos:,, 50-387, 50-388

License Nos:

NPF-14, NPF-22

Report Nos.:

50-387/98-05, 50-388/98-05

Licensee:

Pennsylvania Power and Light Company

Facility:

Susquehanna

Steam Electric Station

Location:

Salem Township, Luzerne County, Pennsylvania

Dates:

September 14- October 2, 1998

Inspectors:

Roy L. Fuhrmeister, Sr. Reactor Engineer

Electrical Engineering Branch

Ram Bhatia, Reactor Engineer

Electrical Engineering Branch

Kenneth Kolaczyk, Reactor Engineer

Civil, Mechanical and Materials Engineering Branch

Frank Amer, Reactor Engineer

Systems Engineering Branch

Alan Blarney, Resident inspector

Susquehanna

Steam Electric Station

Approved by:

David C. Lew, Acting Chief

Electrical Engineering Branch

Division of Reactor Safety, Rl

98ii240054 98iii3

PDR

ADOCK 05000387

6

PDR

0

TABLEOF CONTENTS

PAGE

Executive Summary ..;... ~... ~.... ~........ ~.......................

iii

eport Details ........,. ~.....................,............

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1

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III. Engineering

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E2

Engineering Support of Facilities and Equipment

E2,1

Core Spray System Electrical Design

E2.2

Incorporation of Core Spray System Design Into Technical

Specifications Surveillance Tests .:

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E2.3

Core Spray Surveillance Test Program Implementation ..

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E7

Quality Assurance

in Engineering Activities ..

E7.1

Problem Identification and Resolution

.

E7.2

Core Spray System Flow Discrepancies

E7.3

10CFR50.59 Safety Evaluation Program.....

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V. Management Meetings

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Exit Meeting Summary ..

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PARTIALLISTING OF PERSONNEL CONTACTED

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LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED .. ~, ~............ ~...

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LIST OF ACRONYMS USED.....

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1 9

Executive Summary

This team inspection was conducted September 7 - October 2, 1998 at the site and in the

Region

I office, to assess

the engineering support of the operation of the Susquehanna

Steam Electric Station.

~En inaerin

The core spray system was found to be installed and operated

in a manner consistent with

the design requirements for electrical power supplies as described in the update final safety

analysis report and design basis documents.

Calculations reviewed were adequate to

assure that the components

and control circuits associated with the operation of the core

spray system had sufficient direct current voltage to perform the intended design function.

Refueling testing and emergency diesel load calculations demonstrated

the adequacy of the

electrical power supply to the core spray system components.

(Section E2.2)

Discrepancies identified in surveillance test procedures indicated weak engineering support

in assuring acceptance

criteria bases were sound.

The acceptance

criteria for Unit 1 core

spray test piessure did not take into account system configuration differences between

Units

1 and 2, even though these differences were identified in design calculations.

The

Unit 2 core spray quarterly flow surveillance test inappropriately included a non-

conservative correction factor for which no basis could be identified. Although the

consequence

of these discrepancies

did not result in system inoperability, the above

failures to incorporate the requirements and acceptance

limits contained in applicable

design documents are two examples of a violation of 10 CFR Part 50, Appendix 8,

Criterion III. (VIO 50-387 & 388/98005-01)

(Section E2.2)

The inservice testing program for the core spray system was sound.

Program documents

were found.to be well organized, with appropriate records of relief requests, test deferral

justifications and supporting technical information. Test failures identified during relief

valve testing were appropriately dispositioned.

The industry experience review program

appropriately considered industry information. (Section E2.3)

PP&L's program and process controls for the identification of conditions adverse to quality

were adequate.

The team's review of sixty condition reports indicated that the initiation

threshold was sufficiently low. However, two conditions, which'were not documented,

reflected inconsistency in the initiation of condition reports.

A pressurization of a portion

of Unit 1 core spray discharge piping was not documented

in a condition report, although a

similar problem with the residual heat removal system was documented.

An unexpected

power increase was not document in a condition report; this event was also documented

in

NRC inspection report 50-387&388/98007.

(Section E7.1)

PP&L's resolutions of condition reports were generally acceptable.

However, the

resolutions for two of sixty condition reports were slow, reflecting weak engineering

support.

One issue, involving an instrument inaccuracy deficiency identified in July 1996,

was not thoroughly evaluated and required a revised operability determination.

PP&L was

slow in identifying actions for the final resolution of the problem.

As a result, PP&L missed

an opportunity to make modifications, which were subsequently

determined to be needed,

during the last refueling outages.

The other issue concerned the slow resolution of heat

exchanger fouling in service water systems, which was initiallyidentified in March 1997.

A detailed evaluation of the acceptability of the heat exchanger fouling was not performed

until May 1998, after the initiation of several additional condition reports on the issue.

(Section E7.1)

The resolution of core spray flow concerns reflected a lack of questioning attitude.

PP&L

missed opportunities to identify that the loss of coolant accident (LOCA) analysis did not

reflect the correct core spray flow in the facility's design.

The failure to ensure that the

design basis is correctly translated into the LOCA analysis is a third example of a violation

of the design control requirements of 10 CFR Part 50, Appendix B, Section III. (VIO 50-

3875388/98005-01)

(Section E7.2)

PPRL Nuclear Department Administrative Procedures

provide adequate

guidance to

determine if a 10 CFR 50.59 unreviewed safety question exists.

These documents clearly

delineate the responsibilities for various processes

within the 10 CFR 50.59 pro'gram and

provide adequate

controls for record retention and reporting the results of the evaluations.

The team noted several instances

in which the required 10 CFR 50.59 documentation was

not completed for condition reports dispositioned "use-as-is," as required by program

procedures.

However, technical evaluations provided bases for no unreviewed safety

question.

The failure to implement the administrativ'e procedure for 10 CFR 50.59

evaluations is considered

a minor violation of procedural adherence,

and is not being cited

for formal enforcement action.

(Section E7.3)

.1

Re ort Details

This inspection was conducted as a Safety System Engineering Evaluation, to assess

the

engineering support to the Susquehanna

Steam Electric'Station (SSES) by means of a

detailed review of the design and licensing bases of the core spray system.

The inspection

was conducted during the period September 7 - October 2, 1998, at the site and in the

Region

I office.

III. En ineerin

E2

Engineering Support of Facilities and Equipment

E2.1

Core S

ra

S stem Electrical Desi

n

aO

Ins ection Sco

e

IP 93809

The team reviewed the core spray system (CSS) electrical design as described in

Susquehanna

Steam Electric Station (SSES) Updated Final Safety Analysis Report

(UFSAR) and in the CSS Design Basis Document (DBD). The review included the

assessment

of the electrical equipment design performance as shown in electrical

schematic and control drawings, system calculations and other engineering

documents used to support system performance during normal and accident

conditions.

A plant walkdown of the Unit 1 and Unit 2 CSS and main control room

control panel was performed.

b.

Observation and Findin s

The core spray system, as described in the UFSAR, is required to provide inventory

makeup and spray cooling during large break loss of coolant accidents

(LOCAs) in

which the core is calculated to uncover.

When assisted by the automatic

depressurization

system (ADS), CSS also provides protection for small break

LOCAs. The system consists of two completely independent spray loops.

Each

loop consists of two core spay pumps and motors, a sparger ring, a spray nozzle,

and the necessary

piping, valves, and control instrumentation.

Each loop takes

water from the suppression

pool by suction and delivers water through the sparger

ring into the plenum chamber above the core.

Each core spray pump motor (four in

each unit) is powered from its associated

safety related 4160 volt bus and each unit

safety bus is backed up by its respective emergency diesel generator

(a common

diesel generator for each bus for both units) upon a loss of offsite power.

Desi

n Documentation Review

The inspector reviewed the CSS design of pump motors and applicable system

valves (inboard and outboard injection valves:

HV-E21-004A and 5A; minimum

flow valves:

HV-E21-1F031A and B; and test return line valves to the suppression

pool: HV-E21-1FO15A and B) and other supporting and interfacing equipment, such

as emergency diesel generator (EDG), safety injection actuation system inputs and

1

found it to be adequate

and consistent with the.design and UFSAR requirements.

The review of the power supply requirements, under the degraded voltage condition

were found acceptable for the above equipment.

The inspector found that all

sensors,

relays, wiring, and controls needed to initiate an automatic start of the

CSS were included and consistent with the UFSAR requirements.

The inspectors

noted that each CSS pump motor was appropriately powered from its respective

safety-related 4160 volt bus and backed up by the respective bus designated

EDG.

The power supply requirements for the valves and the control devices of the CSS,

such as motor and its supporting equipment, valves to the reactor coolant system

and the initiation logic sensors,

were adequately designed and powered from the

applicable power supplies required to support CSS operation during normal and

accident operation.

During plant walkdowns the inspector verified that the controls for the CSS pumps,

control valves, the suppression

pool test return and minimum flow valves,'nd

associated

instrumentation were appropriately provided in the main control room to

support the proper operation of the CSS on demand.

Calculation Review

The inspector reviewed design calculations to determine whether the electrical

power supply to CSS loads'and voltage available to the CSS equipment were

adequate

during the worst-case design basis accident, and found no concerns.

However, in one case, during the validation of the system equipment loads and

verification of the cable impedance data in calculation, EC-004-0516, "Plant Voltage

Study Model," used to demonstrate the voltage drop of plant equipment, the

inspector found that PPSL had used

a single conductor impedance value between

load center 1B210 and 1B217 instead of two in parallel installed in the station.

PPSL issued an engineering work order, M80193, on September

21, 1998.

PPSL

stated that since a higher resistance

value was used to determine the voltages in

the station, the results obtained were adequate

and conservative

in this condition.

Overall, this condition was judged by the inspector to have a minimal effect in

voltage results.

The inspector found it acceptable

since the results were slightly

conservative.

PPS.L stated that they would correct this error in their next revision

of this calculation.

The review of the EDG loading calculation results indicated that during the accident

and loss of offsite power (LOOP) condition, the diesel generators were capable of

accelerating accident loads,'nd the design loading on each diesel generator. would

be within the continuous rating of the machine.

The review of the direct current

(DC) electrical system calculations and associated

CSS equipment voltage indicated

no concern, the inspector observed that PPSL had appropriately assumed the

correct loads and assumed

a minimum battery system voltage of 105 VDC at the

end of the cycle and applied appropriate field cable voltage losses in evaluating

voltage drops.

The inspectors concluded that the DC system component and

control circuits associated with the automatic operation of the CSS had sufficient

voltage and were appropriately powered from the respective divisional DC buses to

perform the intended design function.

Surveillance Tests

The inspectors reviewed the results of the May 1998 surveillance test associated

with 18 Months-DG AC-Bus 1A, 1C LOOP/LOCA (SE-124-107, Revision 9), and

found that all CSS components functioned properly including the auto start of the

core spray pump as required.

PPKL had adequately demonstrated

the functionality

of the CSS and other supporting equipment, such as the EDG.

c.

Conclusions

The core spray system was found to be installed and operated in a manner

consistent with the design requirements for electrical power supplies as described in

the update final safety analysis report and design basis documents.

Calculations

reviewed were adequate to assure that the components and control circuits

associated with the operation of the core spray system had sufficient direct current

voltage to perform the intended design function.

Refueling testing and emergency

diesel load calculations demonstrated the adequacy of the electrical power supply to

the core spray system components.

E2.2

Incor oration of Core S

ra

S stem Desi

n Into Technical S ecifications

Surveillance Tests

Ins ection Sco

e

IP 93809

The team performed a walkdown of the Unit 1 and Unit 2 core spray pump rooms.

The team reviewed the core spray system description found in section 6.3 of the

UFSAR, The review also included:

verification of the appropriateness

and

correctness

of design assumptions; confirmation that design bases were consistent

with the licensing bases;

arid verification of the adequacy of testing requirements.

b.

Observations

and Findin s

Lo ic Testin

Logic System Functional test procedure SE-151-001, "18 month functional test of

CS Div I," with one noted exception discussed

below, satisfied the requirements

found within Technical Specification 4.5.1.c.1.

The team found that electrical logic

circuits associated with the throttling function of the injection valves, were

adequately tested.

Low pressure piping protection logic assured that the injection

valves could not open without a confirmatory low reactor pressure signal.

Additionally, the Iow pressure permissive bypass handswitch (HS-15249A/B LO RX

press perm) was appropriately tested to ensure that a common mode failure of the

low reactor pressure permissive logic did not result in the emergency core cooling

system (ECCS) injection valves failing closed.

The Technical Specification 4.5.1.c.1., associated with the I'ogic system functional

test, required ... "a system functional test which includes simulated automatic

actuation of the system throughout its emergency operating sequence

and verifying

that each automatic valve in the flow path actuates to its correct position." The

team could not identify where the system minimum flow valve was tested to ensure

its automatic closure upon an automatic pump start.

Although this interlock was

not tested in the logic system functional procedure, the team determined that it had

been adequately tested within the core spray quarterly flow tests (S0-1/251-A02 5

802). However, it was not included in the acceptance

criteria for the test nor linked

to the technical specification requirement.

Condition report 98-3068 was initiated

to review the last performance of the tests to ensure the valves were stroked

successfully.

An extent of condition review was performed and PPSL determined

that the residual heat removal system logic system functional tests had been testing

the minimum flow valve closing stroke interlock.

PPRL stated that the resolution to

this issue would be resolved within the corrective actions developed in condition

report 98-3068. The team noted that there was no safety consequence

associated

with this finding, as the procedure required sign-offs for closure of the minimum

flow valves during the quarterly flow test.

This failure to ensure that the regulatory

requirement was correctly incorporated in to surveillance test acceptance

criteria is

a violation of the design control requirements of 10 CFR Part 50, Appendix B,

Criterion III; however, because this failure constituted

a violation of minor

significa'nce, it is not being cited for formal enforcement action.

The team found the instrumentation and control calibration and functional tests of

the drywell pressure,

vessel water level and core spray system reactor pressure

permissive channels to be consistent with the technical specification requirements.

Core S ra

Technical S ecification Test Pressure

Calculation EC-051-0004, "Core Spray tech spec test pressure," approved on

June 18, 1998, supported the implementation of improved technical specifications,

by developing a correlation between the expected core spray flow rate and vessel

pressure during design basis accidents.

The calculation utilized conservative

assumptions for estimating the total developed head of the core spray pumps, such

as neglecting the line losses between the suppression

pool and the point where the

system test line pressure was sensed.

At the time the calculation was approved, the Unit 1 technical specification test

requirement was ".. ~ a Core Spray test pressure of 269 psig at a corresponding flow

of 6350 gpm." This composite pump operating point represented

the minimum

acceptable

performance of the pumps.

For Unit 2, the conclusion section of

calculation EC-051-0004stated,that

a test pressure of 282 pounds per square inch,

gage (psig), at 6350 gallons per minute (gpm) corresponded

exactly to a vessel

pressure of 105 psig.

This criterion was consistent with the SSES improved

technical specifications, which required that a loop of core spray be capable of

injecting greater than or equal to 6350 gpm into the reactor pressure vessel against

a steam dome pressure greater or equal to 105 psig.

However, the calculation indicated that for Unit 1, because of differences in the

calibrations of the test line pressure instrumentation loop, the same 282 psig

indicated on control room instrumentation, would not assure

a level of pump

performance which conformed to the licensing requirements

in improved technical

specification SR 3.5.1.7.

Table 3A of the calculation, indicated that the vessel

must depressurize to 99 psig before the system would be capable of supplying the

design loop flow rate of 6350 gpm. Therefore, the Unit 1 technical specification

requirement had been technically inaccurate and would not have assured

a flow rate

of 6350 gpm at a steam dome pressure of 105 psig.

On July 27, 1998, PP&L revised the Unit 1 quarterly core spray flow verification

test, SO-151-A02, to reflect a new core spray loop discharge pressure requirement

of 282 psig, at a flow of 6350 gpm which was consistent with Unit 2. However,

the team noted that this change was incorrect, because it failed to recognize the

differences in system configuration between Units

1 and 2, which were delineated

in Calculation EC-051-004.

The failure to implem'ent proper test acceptance

criteria

for Unit 1 core spray system flows and pressures

is the first example of a violation

of the design control requirements of Appendix B to 10 CFR 50.

(VIO 50-387 &

388/98-05-01)

The team determined that the licensee was'taking appropriate actions to revise

associated tests, as necessary.

Because of this discrepancy, the team requested

the last completed quarterly flowtest records for both Units, in order to verify the

actual pump performances were satisfying the technical specification requirements

and to review the test methodologies due to the differences in test line pressure

instrument calibrations.

Overall, the team determined that the pumps were

performing adequately.

Unit 1 Core S ra

Quarterl

Flow Test

PPSL initiated condition report 98-3069 on October 1, 1998, in response to the

team's concerns regarding the validity of the existing Unit 1 test pressure

acceptance

criterion of 282 psig.

PPRL confirmed that no elevation correction

factors had been applied to the Unit 1 instrument and that a correction factor of.

approximately 6.25 psig was required.

The condition report, based on the

methodology of calculation EC-051-0004, stated that a pump discharge pressure of

288 psig versus the 282 psig criteria, was required to demonstrate

an acceptable

level of system performance.

The team compared the latest test performance data

for both Unit 1 core spray loops to this 288 psig criterion and determined that at

least 10 psig margins remained above this value for both divisions.

The condition

report documented that the test line pressure instruments required calibration prior

to performing the next scheduled flow test.

The team found this resolution

acceptable.

0

0

Unit 2 Core S ra

Quarterl

Flow Test

Condition report 98-3070 was initiated on October 1, 1998, due to questions with

the Unit 2 quarterly flow surveillance test acceptance

criteria.

Based on discussions

with IRC Engineering, PPSL determined that the Unit 2 core spray flow surveillance

tests, SO-251-A02 and B02, had been non-conservatively adding a 7 psig

correction factor to the indicated discharge pressure reading, before comparing the

value to the acceptance

criterion of 282 psig.

However, ISC Engineering stated

that the instrument was properly calibrated and no basis existed for this additional

7 psig factor.

The failure to translate the design basis requirements correctly into

surveillance procedure acceptance

criteria constituted a second example of a

violation of design control requirements of Section III of Appendix B to 10 CFR 50.

(VIO 50-387 & 388/98005-01)

A review of the most recent completed surveillance tests indicated that for the

'A'oop

of Core Spray, 277 psig discharge pressure was achieved at 6500 gpm.

Operability assessment

98-3070calculated

the corresponding pressure at the

required flowrate of 6350 gpm and found the pressure to be 282.3 psig. Therefore,

the actual pump performance had margin (.3 psig), albeit greatly reduced, over the

282 psig acceptance

criteria. The proposed corrective action was to revise the

tests to cor'rect the methodology.

The team found the proposed corrective actions

acceptable.

Core S ra

s stem res onse time testin

Licensin

basis assum

tions

UFSAR Table 6.3-1A (Event Scenario for 100% design basis accident suction line

break), describes,

in part, the nominal input assumptions

utilized for the co're spray

system parameters for the limiting design basis accident (DBA) recirculation pump

suction line break.

The core spray pumps were at rated speed at 40 4 seconds

after the design basis suction line break.

When the pumps 'accelerate to rated

speed and reactor pressure drops below the core spray pump shutoff head, flow will

commence to the vessel through the core spray injection valves HV-152F005A/B.

The flow through the injection lines is detected by flow switch FIS-E21'-1N006A/B,

which sends

a close signal to the minimum flow valve HV-152-F031A/8, The team

noted that UFSAR Table 6.3-1A timeline had not documented the minimum flow

valve closure assumption and, therefore, it was not clear whether the associated

diversion of flow (i.e., bypass flow) was specifically accounted for in the LOCA

analysis.

In response to this concern, on September 23, 1998, PPSL initiated condition

report 98-3010, specifically to address the discrepancy that the design basis

accident nominal input assumptions

assumed full core spray flow to the Reactor

pressure vessel (RPV) at 10.1 seconds after CSS pumps achieve rated speed,

whereas the minimum flow valve closing stroke time was 14 to 20 seconds.

Operability assessment

CR 98-3010, concluded that the actual flow delivered to the

RPV would be greater than that assumed

in the ECCS analysis even with a

..maximum flow deficiency of 200 gallons created by the minimum flow path

diversion.

The team concurred that the minimum flow path diversion did not

invalidate the input assumption of core spray at rated flow in 50.5 seconds, found

in Table 6.3-1A. This was based on a review of diesel generator response time

tests, core spray pump start logic and the expected vessel pressure response for

the limiting suction break event.

Actual core spray injection flow would be

expected to occur at a nominal 30 seconds versus the assumed 40 second time

documented

in the DBA suction line break timeline. As such, the core flow deficit

created by the minimum flow path diversion, would be accounted for by the

additional 10 seconds of flow not taken credit for by the LOCA analysis.

Therefore,

the minimum flow path deficit was bounded by other conservatisms

in the analysis.

The team made the observation that the minimum flow path diversion, when

accounted for, reduced other conservatisms

inherent in the analysis.

PPSL, as part

of their evaluation under condition report 98-3010, stated that an action item will

be performed to review and revise, as appropriate, the SSES design and licensing

documents to assure the licensing basis is accurately characterized.

At a minimum,

the evaluation would consider a change to the SSES UFSAR to identify the

maximum allowable stroke time for the core spray minimum flow valves.

. Additionally, if any change is required to the LOCA analysis time line, appropriate

revisions will be made.

C.

Conclusion

Discrepancies identified in surveillance test procedures indicated weak engineering

support in assuring acceptance

criteria bases were sound.

The acceptance

criteria'or

Unit 1 core spray test pressure

did not take into account system configuration

differences between Units

1 and 2, even though these differences were identified in

design calculations.

The Unit 2 core spray quarterly flow surveillance test

inappropriately included a non-conservative correction factor for which no basis

could be identified. Although the consequence

of these discrepancies

did not result

in system inoperability, the above failures to incorporate the requirements and

acceptance

limits contained in applicable design documents are two examples of a

violation of Section III of Appendix B to 10 CFR 50.

(VIO 50-387 5 388/98005-01)

E2.3

Core S ra

Surveillance Test Pro ram lm lementation

Ins ection Sco

e

The inspector compared the core spray surveillance test program to system testing

requirements and performance criteria, described in the Susquehanna

Technical

Specifications (TS), UFSAR, and Inservice Test (IST) program.

To assess

how PP5L

dispositioned deficient conditions identified during surveillance testing, the inspector

reviewed a sample'of condition reports written during the performance of IST

activities.

Finally, to determine how PPS.L responded to industry events in the IST

area, the inspector reviewed what action, if any, PPRL took in response to NRC

Information Notices (IN)s that discussed

IST program issues.

Observations and Findin s

PPSL was implementing the second 10-year interval of the IST program as

described in program submittals to the NRC dated June 30 and December 29,

1974. The submittals included requests for relief from several American Society of

Mechanical Engineers (ASME) Boiler and Pressure

Vessel Code (Code) requirements,

and incorporated PPSL responses to the regulatory positions contained in Generic Letter (GL) 89-04, "Guidance on Developing Acceptable Inservice Test Programs."

.

An NRC letter, dated April 26, 1995, forwarded the safety evaluation report (SER)

which provided the results of the NRC staff's review of the Susquehanna

IST

  • program.

'he

Susquehanna

IST program was described in administrative procedure

NDAP-QA-0423, "Station Pump and Valve Testing Program."

Testing was

performed pursuant to Section XI of the Code (1989 Edition), which incorporated by

reference Parts 6 (OM-6) and 10 (OM-10) of ASME/ANSI OMa-1988 for pumps and

valves, respectively, and Part

1 (OM-1) of ASME/ANSI OM-1987 for pressure relief

devices.

Design information and test requirements for specific components, relief

requests,

and test deferral justifications were contained in detailed program plans.

Supporting technical details were contained in sub-tier procedures, calculations, and

engineering specifications.

The inspectors found the program documents to be well organized, cross-

referenced,

and readily available.

Program scope was adequate with the correct

number of core spray components included in the IST program.

Code relief requests

were well supported and implemented in accordance with program guidance.

Relief valves installed in the core spray system were tested in accordance with

.

ASME code requirements.

Test failures identified during relief valve testing, were

appropriately dispositioned.

As-part of its industry experience review program,

PPRL had appropriately considered the information contained in NRC Information

Notices including 97-90, "Use of Nonconservative Acceptance Criteria in Safety

Related Pump Surveillance Tests," and 97-09, "Inadequate

Main Steam Safety

Valve Setpoints and Performance

Issues Associated With Long MSSV Piping," for

applicability to the Susquehanna

IST program.

Conclusions

The inservice testing program for the core spray system was sound.

Program

documents were found to be well organized, with appropriate records of relief

requests, test deferral justifications and supporting technical information. Test

failures identified during relief valve testing were appropriately dispositioned.

Industry experience review program appropriately considered industry information.

E7

Quality Assurance in Engineering Activities

E7.1

Problem Identification and Resolution

a0

Ins ection Sco

e

IP 40500

The team reviewed PPS.L's overall program and process for the identification and

'resolution of nuclear safety issues as they related to the Operational Quality

Assurance

Program required by 10 CFR 50, Appendix B, and as described in the

UFSAR, Section 17.2, "Quality Assurance During the Operational Phase."

The team

focused mainly in two areas,

The first area reviewed involved selected portions of

the upper tier program documents, Operational Policy'Statements

(OPS) and the

Nuclear Department Administrative Procedures

(NDAP). In addition, the team

focused specifically on condition reports issued on the core spray system and other

condition reports that were generated

during the inspection period.

Focusing on

these areas, the overall performance of the problem identification program was

assessed.

b.

Findin s and Observations

Corrective Action S stem

Operational Policy Statement OPS-5, Deficiency Control System, Rev. 8, dated

4/3/98, provided the overall purpose and responsibilities of the condition report (CR)

program.

NDAP-QA-0702, Revision 4, dated 5/12/98 and Revision 5, dated

9/25/98 provided the current PPSL process for the CR Program.

The team

determined that PPSL implementation of a program to identify, correct and prevent

recurrence of conditions adverse to quality was acceptable.

However, the following

'weaknesses

were identified during the inspection.

Initiation of Condition Re orts

H

Review of approximately sixty condition reports demonstrated that the initiation

threshold was sufficiently low. However, in the previous three months, the NRC

identified two events in which PPRL did not generate

a condition report.

The first

event involved the Unit 1 Core Spray Injection Check Valve HV152F006A. This

check valve did not form a tight seal and allowed reactor pressure to slowly

pressurize the Division I core spray discharge piping. This condition started after

the recent Unit 1 startup from the tenth refueling outage and stopped pressurizing

prior to mid-September 1998. The Unit 1 Residual Heat Removal (RHR) Division I

and Division II discharge Check valves also had experienced similar problems;

however, condition report 96-2028 evaluated the acceptability of this RHR

condition.

PPSL does not plan to initiate a condition report for the Core Spray

Injection Check Valve, because this condition is no longer present.

Since no CR

was initiated on the CSS discharge piping pressurization,

no reason for the

commencement

nor cessation of the'eakage

was ever determined.

10

The second issue involved an unexpected power increase that occurred on June 26,

1998, during a startup.

In this event the reactor operator inserted

a control rod

several notches to terminate the event.

A condition report was not initiated for this

event.

This event reoccurred six days later during a subsequent

reactor startup,

and the reactor tripped when two reactor operators mis-ranged intermediate range

monitors (IRMs). This event is discussed

in detail in NRC inspection report

IR 50-387 and 388/98-07.

The Operational Experience. Services Screening and Corrective Action Team (CAT)

Meetings were observed and found acceptable.

Corrective Action Reviews

The team reviewed condition reports (CRs) that were in various stages of closure to

determine whether identified issues were being dispositioned appropriately.

This

review identified two condition reports in which PPSL was slow in implementing

corrective actions to ensure the plant was within the design and licensing bases.

Low Pressure

Coolant Injection (LPCI) / Core Spray (CS) Low Pressure

Permissive Instrumentation

FSAR Section 7.6.1a.3.3.1 states that "The LPCI injection valves E11-F015

and E11-F017; and the core spray system injection valves E21-F004 and

E21-F005 are interlocked with a reactor pressure low signal which protects

the system from overpressurization

by not allowing these valves to open

until reactor pressure

is below the system design pressure."

On July 16,

1996, PP5L identified and documented

in CR 96-0905, that (1) the LPCI

injection valves may open above the system design pressure of 450 psig,

when instrument uncertainties were considered

and (2) that the nominal trip

setpoint ranges may exceed the capabilities of the installed instruments.

The

LPCI injection valves must consistently open below the RHR system design

pressure (450 psig) and above the reactor pressure

assumed

in the LOCA

analysis (Reactor Pressure of 400 psig).. CR 96-0905 concluded that the

LPCI valves could be given an open signal at a reactor pressure

corresponding to 477 psig, which is 27 psig above the RHR design pressure..

A review of past instrument calibrations determined that several of the as-

found setpoint were above the LPCI design pressure.

PPRL performed an

operability determination (OD) which concluded that opening of the

RHR'njection

valves, at a reactor pressure of 490 psig, would maintain the piping

stresses

within the code allowable stresses.

11

In June 1997, PP&L initiated CR 97-2013 to document that the previous

analysis performed under CR 96-0905 did not account for static head

pressure differences between the elevation of the LPCI/CS injection valves

and the pressure tap utilized for this low pressure permissive interlock.

CR 97-2013 concluded that the existing pressure instrumentation for control

of the LPCI/CS low pressure permissive interlock does not provide the

needed setpoint accuracy.

A second operability determination was

completed that evaluated

a new maximum pressure that could be seen in the

RHR system and 'determined that the system would not exceed code

allowable stresses.

The corrective actions for this CR include modifications

to replace the LPCI/CS low pressure permissive instrumentation.

The

modifications are 97-9075 for Unit 1 (targeted for installation'during the

2000 refueling outage), and 97-9076 for Unit-2 (targeted for installation

during the 1999 outage).

A lack of rigor in the evaluation of CR 96-0905

resulted in not identifying and evaluating at that time, the static head and

instrument accuracy issues which contributed to the potential for

overpressurizing piping connected to the reactor vessel.

This lack of rigor

resulted in a missed opportunity to implemented these modifications, which

were identified as needed for final resolution by the licensee, during the

recent refueling outages,

Core Spray Room Cooler and Residual Heat Removal Service Water (RHRSW)

Heat Exchanger Cleanliness Control

PPRL Design Basis Document DBD009- ESW, RHRSW, and Ultimate Heat

Sink, Section 2.10.4.1, discusses

the periodic inspection of heat transfer

components to ensure adequate

heat transfer capacity is maintained.

The

Core Spray Room Coolers are inspected utilizing PPSL specification H-1004-

Heat Exchanger/Condenser

Inspection and Condition Assessment

and the

RHRSW Heat Exchangers

are cleaned utilizing specification H-1001 - Heat

Exchanger/Condenser

Tube Cleaning at SSES.

On March 19, 1997, CR 97-

0771 documented that the Unit 2 Core Spray Room Coolers (2E231 A/C) did

not meet the required cleanliness requirements

as specified in specification,

H-1004, paragraph 6.6.1.1.

The cleanliness requirements were not met

because

the room cooler tubes were coated with a thin layer of a hard brown

material that could not be removed.

The operability determination for CR 97-

,0771 was weak in that it did not quantify the effects of this degraded

condition, and the final action plan documented that this condition would be

dispositioned "use-as-is" in CR 97-0980.

On March 22, 1997, CR 97-0801 documented that the Unit 2 "A" Residual

Heat Removal Service Water (RHRSW) heat exchanger (2E-205-A) did not

meet the requirements of specification H-1001, because

a brown deposit

could not be removed from the inside of the heat exchanger tubes.

The

operability determination for CR 97-0801 again did not quantify the effects

of this degraded condition, and the final action plan again documented that

this condition would be dispositioned "use-as-is" in CR 97-0980.

12

On March 31, 1997, CR 97-0980 documented that the unit 2 "B" RHRSW

heat exchanger (2E-205-B) did not meet the requirements of specification

H-1001, because

a brown scale was still present on the inside of the heat

exchanger tubes.

On June 20, 1997, PLI-83761 was issued in reference to

CR 97-0980. This document identified the brown deposits as manganese

and stated that the deposits were acceptable if the heat transfer properties

were evaluated by Nuclear System Engineering (NSE).

On June 30, 1997,

this condition report was dispositioned without (1) a "Use-as-is" disposition,

(2) an extent of condition review, and (3) a detailed evaluation of the heat

exchangers

operability. The action plan developed in CR 97-0980 only

included plans to (1) include new tooling in the future cleaning of heat

exchangers

and (2) removal of the manganese

from the previously identified

heat exchangers

by May 1999.

On September 17, 1997, Nuclear Assurance Services (NAS) initiated CR 97-

3199 to document that CR 97-0771 and CR 97-0801 were closed with the

expectation that CR 97-0980 would disposition these conditions as "use-as-

is."

CR 97-0980 documented that an acceptable

means of cleaning the

manganese

is available, but did not include a "use-as-is" disposition.

PP5L

dispositioned CR 97-3199 as "use-as-is," but did not include a 10 CFR 50.59 safety determination as required by NDAP-QA-0702, rev. 3 to review

the existing conditions against the licensing basis.

The RHRSW heat

exchanges

remained in this condition, without a detailed evaluation,

documented,

until May 1998.

In May, CR 98-1532 identified that the Unit 1

"B" RHRSW heat exchanger tube cleanliness did not meet the acceptance

criteria in specification H-1001. This CR provided a detailed evaluation of

the conditions of the RHRSW heat exchangers

and found the heat

exchangers to be operable, but degraded.

A period of approximately

14 months elapsed between the time that initial fouling of the RHRSW heat

exchangers were identified until a detailed evaluation was performed.

In

addition, a 10 CFR 50.59 review was not performed as required on "use-as-

is" dispositions in late 1997.

Conclusions

PPRL's program and process controls for the identification of conditions adverse to

quality were adequate.

The team's review of sixty condition reports indicated that

the initiation threshold was sufficiently low. However, two conditions, which were

not documented, reflected inconsistency in the initiation of condition report's.

A

pressurization of a portion of Unit 1 core spray discharge piping was not

documented

in a condition report, although a similar problem with the residual heat

removal system was documented.

An unexpected power increase was not

document in a condition report; this event was also documented

in NRC inspection

report 50-3875388/98007.

13

PPS.L's resolutions of condition reports were generally acceptable.

However, the

resolutions for two of the sixty condition reports were slow, reflecting weak

engineering support.

One issue, involving an instrument inaccuracy deficiency

identified in July 1996, was not thoroughly evaluated and required a revised

operability determination.

PPRL was slow in identifying actions for the final

resolution of the problem.

As a result, PPSL missed an opportunity to make

modifications, which were subsequently determined to be needed, during the last

refueling outages.

The other issue concerned the slow resolution of heat exchanger

fouling in service water systems, which was initially identified in March 1997. A

detailed evaluation of the acceptability of the heat exchanger fouling was not

performed until May 1998, after the initiation of several additional condition reports

on the issue.

E7.2

Core S ra

S stem Flow Discre ancies

ao

Ins ection Sco

e (IP 40500)

The inspector reviewed the resolution of CR 97-2874, and the corrective actions

planned for CR 98-1197, along with the information in PP5L Calculation EC-051-

0004, Rev. 2, "Core Spray Tech Spec Test Pressure."

b.

Observations

and Findin s

In August 1997, the SSES resident inspectors raised the issue that the flows from

ECCS pumps might not meet accident analysis assumed flows at the lower limit of

diesel generator technical specificatio'n allowable speed.

The pump flows would be

reduced by the lower pump speed caused by the lower frequency supplied to the

electric motors which drive the pumps.

PPSL issued CR 97-2874'to document and

evaluate the condition. Through improved technical specification engineering

research

and subsequent

calculations, PPRL determined that the minimum level of

ECCS pump performance verified by technical specification surveillance tests did

not assure that the flows assumed

in the LOCA analyses were bounded at the

lowest allowable diesel generator frequency.

The results of the evaluation of the

CSS were documented

in calculation EC-051-1006, Rev..0, "Core Spray System:

Determination of Pump Flow at Reduced Emergency Diesel Generator Speeds."

This

calculation determined that the CSS performance did not envelope the flows

assumed

in the accident analysis even at rated frequency (60 Hz). This matter was

dispositioned by PPSL through the adoption of a "licensing position" that diesel

generator governor tolerances

and instrument inaccuracies do not need to be

accounted for in accident analysis calculations, due to existing conservatisms

inherent in the Appendix K methodology, as well as the margin between best

estimate analyses

and the 10 CFR 50.46 limit on peak cladding temperature.

14

In April 1998, CR 98-1197 was issued to document the fact that PP&L had

determined even when actual pump performance at rated frequency (60 Hz) was

used, the core spray system flows assumed

in the LOCA accident analyses were

not enveloped at low reactor vessel pressures.

At the time of this inspection, the

CR was still open.

The OD for this CR addresses

both the potential flow

deficiencies for CSS and RHR system, since the calculation for the RHR had not yet

been completed.

A best estimate analysis was performed, using the methodology

of EC-051-1006, and concluded that there would be a LPCI flow above that

assumed

in the LOCA analysis, and this excess would more than make up for the

CSS flow deficit. The inspector was unable to review the methodology in EC-051-

1006, since the calculation has been canceled,

and withdrawn from the PP&L

records system.

Calculation EC-051-0004, Rev. 2, "Core Spray Tech Spec Test Pressure," was

issued June 18, 1998, to support the implementation of ITS. During the

engineering research for ITS, and that conducted to resolve CR 97-2874, the basis

of the Unit 1 technical specification CSS flow and pressure acceptance

criteria

could not be located, while PP&L determined those for Unit 2 were based on

preoperational testing results.

The calculation determined that the flow rates

assumed

in the accident analyses for the CSS would not be met in all cases

(particularly at low vessel pressures),

but would provide an interim basis for Unit 1

and 2 surveillance test acceptance

criteria while CR 98-1197 was resolved.

The

calculation stated that future revisions were probable, and that a new "licensing

basis" flow for the core spray system would be developed based on the actual

system performance.

This new "licensing basis" flow would provide the final

design and testing basis CSS test pressure,

as well as define the CSS accident flow

profile.

During review of Calculation EC-051-0004,

the inspector determined that the

LOCA analysis assumed

CSS flows of up to 8143 gpm with the reactor vessel and

drywell pressures

equalized.

The CSS DBD states that the system is orificed to limit

CSS flow to 7900 gpm, since spray sparger discharge patterns become erratic,'nd

adequate

core cooling can not be assured,

at flows above 8000 gpm per loop.

PP&L had not identified this error in the accident analysis assumptions,

only that

there was a disparity between the flow achievable by the system, and that assumed

in the accident analysis.,

The team concluded that the lack of questioning attitude,

associated with the resolutions for CR 97-2874 and CR 98-1197, reflected missed

opportunities to identify this error.

The failure to ensure the adequacy of the LOCA analysis is a violation of Section III,

"Design Control," of Appendix B to 10CFR 50, which requires that measures

be

established to ensure that the design basis is correctly translated into specifications,

drawings, procedures

and instructions.

(VIO 50-387 & 288/98005-01)

15

c.

Conclusions

The resolution of core spray flow concerns reflected a lack of questioning attitude.

PP&L missed opportunities to identify that the loss of coolant accident analysis did

not reflect the correct core spray flow in the facility's design.

The failure to ensure

that the design basis is correctly translated into the LOCA analysis is a third

example of a violation of the design control requirements of 10 CFR Part 50,

Appendix B,Section III. (VIO 50-387&388/98005-01)

E7.3

10CFR50.59 Safet

Evaluation Pro ram

aO

Ins ection Sco

e (IP 37001)

The team reviewed PP&L's implementation of the 10 CFR 50.59 Program.

This

review involved selected portions of Nuclear Department Administrative Procedures

(NDAPs).

In addition, the team reviewed core spray plant modifications, procedure

changes,

Replacement Item Evaluations and condition reports.

The team also

reviewed UFSAR changes,

previous 10 CFR 50.59 determinations and 10 CFR 50.59 determinations performed under the recently revised NDAP-QA-0726,

Revision 3.

Focusing on these areas allowed the overall performance of PP&L's

10 CFR 50.59 Program to be assessed.

b.

Findin s and Observations

Procedures

and Controls

NDAP-QA-0726, Revision 3, "10 CFR 50.59 Evaluations," and NDAP-QA-0730,

Revision 1, "Implementation and Control of Licensing Documents," provided

adequate

guidance, when combined with training, to determine if an unreviewed

safety question (USQ) existed.

These documents also clearly delineate the

.

responsibilities for various processes

within the 10 CFR 50.59 program,

In addition,

these documents provided adequate

controls for record retention and reporting the

results of 10 CFR 50.59 evaluations.

Im lementation of the 10 CFR 50.59 Process

The 10 CFR 50.59 determinations

and evaluations reviewed by the team were

adequate.

These team focused on recent 10 CFR 50.59 determinations and

evaluations associated with the core spray system and core spray support systems.

Overall, these evaluations were acceptable,

in ensuring that the technical issues

were fully addressed,

and that an adequate

engineering basis existed to determine

no unreviewed safety question existed.

16

However, the'team noted that the administrative implementation of the 10 CFR 50.59 process was found to be weak with regard to condition reports that

disposition deficiencies as "use-as-is."

Of the eight condition reports reviewed, in

which the licensee dispositioned as "use-as-is,".the team noted that six did not

contain completed forms documenting

a 10 CFR 50.59 determination or evaluation,

as required by procedure NDAP-QA-0726.

98-0839

Laminar indications found in the stainless steel cover plate on the Unit

1 RCIC Room Cooler (1E228B).

PP&L engineering determined that

these indications did not reduce the strength of the plate and were

acceptable.

98-0890

Internal cleanliness inspection on the D-1 intercooler noted a foreign

material identified as general purpose silicone sealant (RTV 102/ RTV

108) inside the air side of the cooler.

Maintenance Engineering and

the Diesel vendor concluded that this will not effect the performance

of the engine.

98-0991

During maintenance activities under work authorization (WA) No.

A70350, an unexpected wear pattern was identified on 7L and 8L

intake cams of "D" emergency diesel generator.

PPRL engineering

and the vendor concluded that these wear marks were the result of a

vendor applied coating.

There were no similar indication on other

diesel generators.

98-1 683

A review of the previous Unit 1 inspections of the H4 and H5 shroud

welds revealed that a 62 inch long crack exists in the shroud H5 weld

centered at the exact location of the vertical weld at azimuth

135 degrees.

The vertical welds have never been inspected.

The

inservice inspection (ISI) and analysis conducted at the completion of

the Unit 1 tenth refueling outage determined that integrity of

the'hroud

was acceptable.

98-1 81 5

During Scheduled

ISI inspections on Unit 1, four ultrasonic indications

  • were identified on the core shroud weld H4. The ISI inspection and

analysis conducted at the completion of the Unit 1 tenth refueling

outage determined that integrity of the'shroud was acceptable.

98-2082

WA C73770 required 4 quality control verifications.

One of the four

was not verified by QC, however, field support engineering performed

the verification and determined the condition to be acceptable,

In addition to these examples,

CR 97-3199, was dispositioned "use-as-is" and did

not contain a 10 CFR 50.59 determination or evaluation.

This is discussed

in the

condition reporting section of this report.

17

PPRL initiated condition report 98-3076 to investigate this issue and determine

appropriate corrective actions.

This violation of the requirement of NDAP-QA-0726

was considered to be minor in nature, and is not being cited for formal enforcement

action.

C.

Conclusions

PPRL Nuclear Department Administrative Procedures

provide adequate

guidance to

determine if a 10 CFR 50.59 unreviewed safety question exists.

These documents

clearly delineate the responsibilities for various processes

within the 10 CFR 50.59

program and provide adequate

controls for record retention and reporting the results

of the evaluations.

The team noted several instances

in which the required 10 CFR 50.59 documentation was not completed for condition reports dispositioned "use-

as-is," as required by program procedures.

However, technical evaluations provided

bases for no unreviewed safety question.

The failure to implement the

administrative procedure for 10 CFR 50.59 evaluations is considered

a minor

violation of procedural adherence,

and is not being cited for formal enforcement

action.

V. Mana ement Meetin s

X1

Exit Meetin

Summa

'- The results of the inspection were discussed

at an exit meeting conducted at the site on

October 2, 1998.

During the inspection, some of the drawings, specifications, and calculations reviewed by

the team were identified as proprietary information. All copies of documents used by the

team were destroyed after the end of the inspection.

PARTIALLISTING OF PERSONNEL CONTACTED

Penns

Ivania Power and Li ht

G. Miller, General Manager, Nuclear Engineering

R. Pagodin, Manager, Nuclear System Engineering

M. Simpson, Manager, Nuclear Technology

T. Gorman, Project Manager, Nuclear Engineering

J.

Kenney, Supervisor, Nuclear Licensing

'R. Prego, Supervisor, Site Surveillance Services

R. Wehry, Supervising Engineer, licensing

Nuclear Re viator

Commission

W. Axelson, Deputy Regional Administrator

R. Crlenjak, Deputy Director, Division of Reactor Projects

C. Anderson, Chief, Reactor projects Branch 4

W. Ruland, Chief, Electrical Engineering Branch

K. Jenison, Senior Resident Inspector

J.

Richmond, Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-3875.388/98005-01

Three examples of failures to correctly translate regulatory

requirements

and design bases into test acceptance

criteria or

accident analyses.

Closed

None

Discussed

None

LIST OF ACRONYMS USED

ADS

ASME

CFR

CR

CSS

DBA

DC

ECCS

EDG

ESSW

FSAR

GL

GPM

IP

ISI

IST

ITS

LDCN

LOCA

LPCI

NRC

OD

PPS.L

PSIG

QC

RHRSW

RWCU

SER

SSES

TS

UFSAR

WA

Automatic Depressurization

System

American Society of Mechanical Engineers

Code of Federal Regulations

Condition Report

Core Spray System

Design basis Accident

Direct Current

Emergency Core Cooling System

Emergency Diesel Generator

Essential Safeguards

Service Water

Final Safety Analysis Report

NRC Generic Letter

Gallons per Minute

Inspection Procedure

Inservice Inspection Program

Inservice Testing Program

Improved Technical Specifications

Licensing Document Change Notice

Loss of Coolant Accident

Low Pressure

Coolant Injection

Nuclear Regulatory Commission

Operability Determination

Pennsylvania Power and Light

Pounds per Square Inch, Gage

Quality Control

Residual Heat Removal Service Water

Reactor Water Cleanup

Safety Evaluation Report

Susquehanna

Steam Electric Station

Technical Specifications

Updated Final Safety Analysis Report

Work Authorization

4~

4

I