ML17158B940
| ML17158B940 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 01/29/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17158B938 | List: |
| References | |
| 50-387-96-13, 50-388-96-13, NUDOCS 9702100146 | |
| Download: ML17158B940 (69) | |
See also: IR 05000387/1996013
Text
U. S. NUCLEAR REGULATORY COMMISSION
REGION
I
Docket Nos:
License Nos:
50-387, 50-388
Report No.
50-387/96-1 3, 50-388/96-1 3
Licensee:
Power and Light Company
2 North Ninth Street
Allentown, Pennsylvania
19,101
Facility:
Susquehanna
Steam Electric Station (SSES)
Location:
P.O. Box 35
Berwick, PA 18603-0035
Dates:
December 3, 1996 through January 13, 1997
Inspectors:
K. Jenison,
Senior Resident Inspector
B. McDermott, Resident Inspector
K. Kolaczyk, Reactor Engineer,
Approved by:
Walter J. Pasciak, Chief
Projects Branch 4
Division of Reactor Projects
9702i00i46 970i29
ADGCK 05000387
8
EXECUTIVE SUMMARY
Sus'quehanna
Steam Electric Station, Units
1 & 2
NRC Inspection Report 50-387/96-13, 50-388/96-13
This integrated inspection included aspects of licensee operations,
engineering,
maintenance,
and plant support.
The report covers
a 6-week period of resident inspection;
in addition, it includes the results of an announced
inspection by a regional inspector.
~Oerations
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The activities performed by the operators during this inspection period were
determined to be conservative,
in accordance
with the applicable SSES procedures,
and in compliance with applicable technical specifications
(TSs).
Licensed plant
. '- control operators
(PCOs) were well able to,communicate the status of their Unit and
the rational for planned and completed actions.
One instance of excellent and two instances of weak nuclear plant operator
performance were observed/reviewed
during this inspection period.
One
performance error involved the mis-alignment of nonsafety related equipment with
the potential to impact the stable operation of Unit 2. The second issue involved
the improper coordination of a valve alignment for Unit 2 safety related equipment.
Licensee corrective actions included positive behavior modification and the
communication of the performance issues to other operating shift personnel.
The
root cause and corrective action efforts of the Operations Department employed
diverse diagnostic methods, were aggressively performed and were professionally
executed.
The interaction between PPSL management
and staff at a PORC meeting on
January 2, 1997, was viewed as constructive by the inspector.
Of import, the
interaction led to the discussion of a generic issue concerning the control of doors
for station equipment and plant areas.
Although PORC's activities were considered
positive, the inspector viewed the absence
of generic consideration for the blocked
open cabinet door in the Condition Report (CR) resolution to be a weakness
in
implementation of the corrective action process.
A conversion constant affecting the reactor water cleanup system flow value used
to calculate the average core thermal power (CTP) was not correct.
The error is
thought to have existed since initial startup of both Susquehanna
Units and results
'n
the indicated CTP being one mega-watt thermal greater than actual.
This error is
considered to be of low safety significance when compared to the licensed CTP of
3441 MW~, even when combined with other CTP calculational problems identified
in the last two years.
Exceeding the licensed CTP by a small amount was treated
as a non-cited violation.
The licensee failed to control the placement of equipment near safety related
equipment (4.16 kV switchgear) in accordance
with plant procedures.
Adequate
corrective actions were undertaken
by the licensee after the issue was identified to
them.
This constitutes
a minor violation and was treated as a non-cited violation.
Maintenance
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Hydrogen/oxygen
analyzer maintenance
activities did not completely document the
as-left condition of the equipment.
Therefore, it was not possible to determine post
maintenance
operability of the equipment without supporting discussions with the
SSES maintenance
and nuclear system engineering
personnel.
The failure to
adequately document the performance of safety related maintenance
and the basis
of equipment operability constitute
a minor violation and was treated as a non-cited
violation.
k
PP&L has a preventive maintenance
backlog reduction plan in place that is being
monitored by SSES Plant Management.
Based on a sample review of the backlog,
the inspector independently
verified the licensee's determination that no overdue
activities affect the environmental qualification of the equipment.
An undocumented
modification/replacement
of a Unit 2 standby liquid control pump
accumulator was identified by the inspector.
The licensee's
response to the
technical issue was quick and complete.
The safety impact of the identified
replacement was low because the capacity of the accumulator met its system
design requirements.
PP&L's repeated failure to provide adequate
control for high energy line break room
doors, blocked open in support of maintenance,
was considered
a violation of
10 CFR 50 Appendix B, Criterion XVI, Corrective Action.
During the performance of standby gas treatment system maintenance,
power was
returned inside a blocking permit boundary without meeting the requirements of the
licensee's tagging and permit procedures.
Although no personnel injury or
equipment damage occurred, this is considered
a violation of TS 6.8.1,
"Procedures".
~En ineerin
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Standby liquid control pump flow calibrations use unborated water as a medium.
The calibration water is discharged through a recirculation flow path. At the
completion of the test, the normal discharge flow path into the vessel is left filled
with the unborated water.
The licensee was able to produce design basis
documentation that takes into account
a 30 second delay from the time of boron
injection initiation to the time that boron actually enters the core.
These
calculations conservatively account for the unborated water left in the injection line
following the surveillance flow testing.
~
The licensee responded to a violation involving control rod drive mechanism
replacement
in a aggressive
manner.
The licensee's root cause evaluation was
aggressive
'and insightful in that it identified a number of subtle contributions to the
event, was quick in its evaluation of the event, involved a large cross section of
SSES technical expertise and was subjected to the routine high standards
of the
~
Power 5 Light (PPRL) established
a motor-operated
valve (MOV)
program that met their commitments to Generic Letter (GL) 89-10 "Safety-Related
Motor-Operated Valve Testing and Surveillance."
~
The design basis capability of MOVs was adequately
established
through the
performance of in-situ testing, analysis and most notably through use of the Electric
Power Research Institute (EPRI) Performance
Prediction Model (PPM) software.
PPSL established
a large data base of MOV performance characteristics
in tracking
and trending programs and used the information to improve MOV performance
and
detect degradation.
~
Although PP5L demonstrated
safety-related
MOVs had adequate
design margin, the
methodology PPSL used to account for the effects of load sensitive behavior (LSB)
was inconsistent with the general understanding
of the phenomenon.
Specifically,
PPRL assumed
LSB was a random occurrence when developing the switch settings
for MOVs. It is the NRC's position that industry testing has revealed LSB tends to
reduce motor actuator thrust output under dynamic conditions as a result of
increased
stem friction and, therefore, is a predictable occurrence which is valve-
specific.
~
When developing valve factors for 42 untested Anchor Darling gate valves, PPSL
used data obtained from the EPRI flow loop test program that may not be applicable
to Susquehanna.
However, re-evaluation of available valve factor showed adequate
margin.
~
The analytical approach
used to reduce the number of installed mechanical snubbers
was thorough; the design guide used was comprehensive
and provided detailed
criteria for pipe support analysis.
~
The licensee failed to adequately control health physics technician overtime during
the most recent Unit 1 outage.
In approximately 60 cases the licensee did not meet
the guidelines in Technical Specification 6.2.2, "Unit Staff." This licensee identified
and corrected violation was treated as a non-cited violation.
TABLE OF CONTENTS
EXECUTIVE
UMMARY
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I. Operations
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Conduct of Operations .................... ~............
01.1
Operator's
Response
to Transient Conditions
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01.2
Non-Licensed Nuclear Plant Operator Field Performance
01.3
Effectivene'ss of Licensee Controls in Problem Resolution
Operational Status of Facilities and Equipment ................
02.1
Core Thermal Power Calculation Errors
02.2
Storage of Transient Equipment Located Near Safety Related
Equipment
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Operations
Pi'ocedures
and Documentation
03.1
Posting of Notices to Workers
Quality Assurance
in Operations ..
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07.1
Review of Third Party Audits
Miscellaneous Operations Issues..........................
08.1
Control Rod Scram Accumulator Alarm
08.2
(Closed) LER 50-387/96-17: Non-Conservatism
in Heat
Balance Calculation
08.3
(Closed) IFI 50-387/94-19-01: Licensee's Abilityto Activate
the Backup Emergency Operating Facility (EOF)
08.4
(Closed) IFI 50-387/95-16-01: Emergency Preparedness
Training
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(Closed) LER 50-387/96-10: Main Steam Line Penetration
Leakage Rate Exceeded Technical Specification Limit ......
08.6
(Closed) LER 50-387/96-11: Secondary Containment Bypass
Leakage Rate Exceeded Technical Specification Limit ......
08.7
(Closed) LER 50-387/96-12: Missed Firewatch...........
08.8
(Update) LER 50-387/96-13: Reactor Condition Change
08.9
(Update) LER 50-388/96-09: 'D'HR Pump Failure
To Start
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M1
Conduct of Maintenance
M1.1
Review/Observation
of Maintenance Activities
IVI1.2 Surveillance Test ActivitySample Reviews
M1.3
Review of Ongoing and/or Emergent Maintenance Activities-
Unit 1 Hydrogen/ Oxygen Analyzer ............
M1.4 Observation of Major Surveillance Testing
- HPCI Quarterly
Flow Surveillance
M1.5
Review of Preventive Maintenance
Backlog .......
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Unit 2 Standby Liquid Control Pump Discharge Accumulator
M1.7
Effectiveness of Licensee Controls for Maintenance
M1.8
Effectiveness of Licensee Controls for Maintenance
I. Maintenance
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TABLE OF CONTENTS (Continued)
M2
M3
Maintenance
and Material Condition of Facilities
M2.1
Maintenance
and Material Condition of Facilities
Maintenance
Procedures
and Documentation .......
lVI3.1
Unit 2 Reactor Building, Elevation 766, Access
0 pe ning
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Miscellaneous
Maintenance
Issues
M8.1
(Closed) Violation 50-387/96-10-02 Control Rod
Mechanism Replacement
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E8,4
E8.5
II. Engineering
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Conduct of Engineering
E1.1
Engineering Problem Resolution
E3
Engineering Procedures
and Documentation ...............
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Unit 2 Standby Liquid Control Pump Discharge Flow Design
Basis
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Replacement
Item Evaluation
(RIE)
E8
Miscellaneous
Engineering Issues
E8.1
Review of the Updated Final Safety Analysis Report (UFSAR)
E8.2
(Closed) URI 50-388/95-20-01: Standby Liquid Control IST
Instrumentation
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(Update) Unresolved Item 50-387/94-14-01, 50-388/94-15-
01: pressure
locking and thermal binding of
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Motor-Operated Valve Program Review
Design Modification Process
and Implementation
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Radiological Protection and Chemistry (RPRC) Controls.........
R6
RP&C Organization and Administration
R6.1
Administrative Requirements for Workers Involved in Safety
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Exit Meeting Summary............
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Drop-in Meeting By PPSL Managers
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39
Re ort Details
Summar
of Plant'Status
Both SSES Units operated at 100% power throughout this inspection period, with a few
exceptions.
Short periods of reduced power operation were made to support maintenance
and equipment related activities, and to support minimum power generation conditions on
the Pennsylvania,
Maryland electrical distribution system.
I. 0 erations
01
Conduct of
Operations'1.1
0 erator's
Res
onse to Transient Conditions
a.
Ins ection Sco
e 71707
The inspector observed
and/or reviewed licensed plant control operator (PCO)
response to the following abnormal conditions:
AR 214-001, l.IPCI Barometric Condenser
Level
AR 015-001, Sodium Particulate Iodine Gas Monitor
In addition, the PCOs'esponse
to routine, immediate conditions were also
observed/reviewed.
b.
Observations
and Conclusions
The activities performed by the PCOs in the control room during this inspection
period were determined to be conservative,
in accordance
with the applicable SSES
procedures,
and in compliance with applicable Technical Specifications (TSs).
The
PCOs were well able to communicate the status of their unit and the rational for
planned and completed actions.
01.2
Non-Licensed Nuclear Plant 0 erator Field Performance
a.
Ins ection Sco
e 71707
The inspector reviewed selected aspects of nuclear plant operator (NPO)
performance during routine activities.
~'Topical headings such as 01, MS, etc., are used in accordance with the NRC standardized
v
reactor inspection report outline.
Individual reports are not expected to address
all outline
topics.
b.
Observations
and Findin s
On December 10, 1996, in support of a high pressure
coolant injection
(HPCI) system draining operation, Drain Recommendation
(DR) 252-001,
HPCI, was performed.
Step 3.4.12 was the responsibility of the PCO to
perfor'm from the control room and steps 3.4.13 and 3.4.14 were the
responsibility of the NPO to perform in the field. The NPO did not ascertain
whether step 3.4.12 was completed prior to performing steps 3.4.13 and
3.4.14.
Consequently,
the NPO performed his steps out of sequence.
This
error resulted in an abnormal alignment of the cooling water to the HPCI
barometric condenser,
a high level in the barometric condenser
vacuum tank,
and a high level alarm.
Performance of step 3.4.12 at the proper time would
have isolated the abnormal flow path by shutting valve HV-256-F059.
The
PCO took the appropriate steps in response
tc; the alarmed condition, and
Condition Report (CR) 96-2197 was issued to document the issue.
The
quick action taken by the PCO limited the safety impact of the personnel
error and did not delay the HPCI pump return to service.
The corrective
actions and root cause evaluation identified in the CR were evaluated by the
inspector and determined to be excellent.
'he
failure to control the alignment of safety related equipment in
accordance
with plant procedures
constitutes
a violation of minor
consequence
and is being treated as a non-cited violation consistent with
Section IV of the NRC Enforcement Policy. This issue is closed.
2.
On December 8, 1996, an NPO attempted to isolate the Unit 2, 'C'ervice
water pump suction valve in order to support scheduled
maintenance.
The
operator incorrectly initiqted the isolation of the Unit 2 'B'ervice water
pump.
When the 'B'uction valve came off of its open seat the control
room received an alarm "B SW PP SUCT VLVNOT FULL OPEN". The PCO
took immediate action to return the 'B'uction valve to its open seat.
The licensee determined that there was no impact on operating equipment
but, classified the event as a "near miss with potentially significant impact to
the Unit." A-human performance causal review and a root cause evaluation
were performed.
In addition, the licensee issued CR-96-2183 to affect
corrective actions.
Because of the potential safety impact from a loss of service water flow
(turbine trip, reactor trip); the inspector reviewed the event, interviewed
selected operators,
and monitored the licensee's corrective actions and root
cause evaluations.
The response
of Operations management
was quick and
extensive.
A root cause of personnel error (failure to implement the
self-checking process) was established
using two different diagnostic
methods.
=Operations management
approached
the corrective action issues
in a responsive
and professional manner.
The corrective actions, which
included positive behavior modification, were well communicated to other
Operations personnel
and were designed to prevent recurrence.
3.
On December 17, 1996, the inspector observed portions of a routine NPO
round in the Unit 2 reactor building.
The NPO performed the tasks required
by his round'sheet.
The inspector noted that the NPO verified the proper
configuration/indication
on a number of additional pieces of equipment that
did not appear on the required round sheet.
The NPO also verified the proper
operation of all fire doors traversed during the tour.
Based on observations
of this NPO tour, the inspector concluded that the NPO demonstrated
an
excellent knowledge of his responsibilities and was very observant of general
equipment conditions.
c.
Conclusions
One instance of excellent and two instances of weak nuclear plant operator
performance were observed/reviewed
during this inspectjon period.
One
performance error involved nonsafety related equipment with the potential to impact
the stable operation of Unit 2. The second issue involved the improper coordination
of a valve alignment for Unit 2 safety related equipment.
Licensee corrective
actions included positive behavior modification and the communication of the
performance
issues to other operating shift personnel.
The root cause and
corrective action efforts of the Operations Department employed diverse diagnostic
methods, were aggressively performed, and were professionally executed.
01.3
Effectiveness of Licensee Controls in Problem Resolution
~ 1
a.
Ins ection Sco
e 71707
The effectiveness of the licensee's controls in identifying, resolving, and preventing
a problem was evaluated during observation of a plant operations review committee
(PORC) meeting for approval of CR 96-2170 on January 2, 1997.
Additional
discussion
regarding PP&L's controls for problem resolution are contained
in Section
E1.1 of this report.
b.
Observations
and Findin s
PORC meeting 97-01-02B was held to review the corrective actions taken and
planned in response to PP&L's discovery (CR 96-2170) that the ground/test devices
for the 4.16 kV emergency safeguard
system
(ESS) switchgear were not considered
in the switchgear's original seismic analysis.
This issue was identified during initial
followup actions for PP&L's discovery that the 4.16 kV switchgear seismic analysis
did not assume
any breakers would be in their racked out or test positions (see
LER 50-387/96-15).
PP&L's review of how the ground/test device is used also
identified that the switchgear cubicle door can not be fully closed and latched (as
per the seismic analysis) with the device's external ground wire in use.
During the PORC review of the CR resolution, the committee raised good technical
and CR process related questions.
The blocked open switchgear cubicle door
aspect of the issue was initiallyof low visibility, however it gained significant
attention after a system engineer questioned the effectiveness of past corrective
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actions for similar problems.
The corrective actions proposed
in the CR 96-2170
resolution did not address whether these similar problems had been evaluated.
Plant management
recognized that the corrective action process
had not captured
several previous events related to blocked open equipment doors.
This
development was well received by plant management
and PORC's consensus
was
that additional work was required in this area.
Approval of the CR resolution was
deferred pending the resolution of PORC comments.
The inspector noted that NRC unresolved
item URI 50-387,388/95-24-01
identified
a similar problem with a blocked open cabinet door that occurred when temporary
monitoring equipment was installed on an emergency diesel generator control panel
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The report discussion noted that certain aspects of temporary equipment
installations, such as electrical separation,
seismic considerations,
and fire
protection, were not being adequately considered.
A related issue concerning
environmental qualification and the control of doors for rooms with high energy line
break (HELB) protection are discussed
in Section E2.1 of this report.
PPRL's
followup of the generic door control issue will be reviewed along with their response
to-the corrective action violation discussed
in section M1.7 of this report.
C.
Conclusions
The interaction between PPSL management
and staff at the PORC meeting on
January 2, 1997, was viewed as constructive by the inspector.
The interaction led
to reconsideration
of corrective actions for a generic issue concerning the control of
all types of doors.
Although PORC's activities were considered
positive, the
inspector viewed the absence of generic consideration for the blocked open cabinet
door in the CR resolution to be a weakness
in implementation of the corrective
action process.
02
Operational Status of Facilities and Equipment
02.1
Core Thermal Power Calculation Errors
aO
Ins ection Sco
e 71707
On December 3, 1996, PPSL identified that an analog computer point affecting the
core thermal power (CTP) calculation was indicating a lower mass flow rate than
expected.
PPS.L calculated that as a result, the CTP may be greater than expected-
by approximately 0.8 mega-watt thermal (MW~) and reported to the NRC that both
SSES Units may have exceeded their licensed CTP limits at some time since initial
startup (Reference EN¹ 31404).
The inspector reviewed this non-conservatism
in
the CTP calculation and reexamined other similar conditions reported by PPSL over
the last two years.
b.
Observations
and Findin s
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Three previous reports of errors in the calculated core thermal power were
reexamined:,
In February 1995, PP&L discovered that inaccuracies
in the Unit 2 feedwater
flow (FW) instrumentation
had resulted in a 0.8 MW error in the calculated
CTP and that on several occasions the eight hour shift average
CTP had
exceeded
the license limit of 3441 MW~. PP&L determined the cause of this
event to be errors in original instrumentation drawings that incorrectly
depicted the location of certain instrument taps.
To bound this inaccuracy
PP&L administratively restricted CTP on Unit 2 to 3440 MW . Unit 1 was
not affected by this problem.
The drawings were corrected and the FW flow
instrument was recalibrated.
In June 1995, PP&L's review of a Unit 2 failed instrument transmitter
identified that the instrument drift which preceded the failure caused
a non-
conservative
influence on the calculated CTP.
Initial follow up to this
discovery found that the 'A'eactor Recirculation (RR) pump indicated
power was higher than expected
and the reactor water cleanup (RWCU) inlet
temperature was indicating low. To bound these instrumentation accuracy
problems PP&L administratively restricted Unit 2 operation to below an
indicated CTP of 3437 MW . These issues were.subsequently
resolved.
In December 1995, PP&L's review of an industry event found that seal purge
flow entering the reactor coolant system from RR and RWCU pumps affected
the CTP and were not accounted for in the CTP calculation.
An
administrative limit of 3439 MW~ was placed on both SSES Units pending
corrective actions.
Corrective actions included development of a design
basis document for the CTP calculation and subsequent
revision of the
calculation determined that the actual CTP output was less than had been
originally calculated.
PP&L retracted their original report of exceeding the
licensed CTP in LER 50-387/95-15-01.
Most recently, on December 4, 1996, PP&L made a 24-hour notification to the NRC
when they determined that the flow conversion constant for RWCU was not correct
and had a non-conservative
impact on the calculated CTP for both SSES Units.
PP&L determined it was likely that both Units had exceeded their licensed thermal
power limit at some time since initial startup due to this error.
Upon identification,
PP&L established
interim administrative controls to reduce the CTP limit by
1 MW
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pending correction of the conversion constant.
PP&L found that an instrument which provides inputs to both the RWCU leak
detection system and the CTP calculation was not providing the CTP calculation an
accurate mass flow rate.
The instrument's output is normalized to standard
temperature
and pressure to facilitate comparison of RWCU inlet and outlet flow
rates for leak detection.
However,- due to the conversion constant error the CTP
'alculation
did not account for the fact that the indicated flow rate provided to it
had been normalized.
Typical RWCU system pressure
and temperature were
assumed
in the CTP calculation.
The difference in conversion constant resulted in
the mass flow rate being approximately 40,000 Ibm/hr lower than actual flow rate.
PPKL'elieves this conversion constant
is the original one supplied by General
Electric and plans to inform other utilities of the potential generic issue via the
Nuclear Network.
The errors in CTP. calculations reported by PP5L over the last two years appear to
be of two types.
The first three errors resulted from instrumentation inaccuracies
caused by errors in their calibration or component failures.
The two most recent
issues resulted from original design errors and may be generic to other boiling water
reactors.
In order to assess
the safety impact, the inspector postulated that these errors were
simultaneously present and assumed
a bounding error of 6.0 MW~ based on the
Unit 2 errors discussed
above.
Relative to the Unit 2 licensed CTP limit of 3441
MW~ the combination of these errors would result the indicated CTP being 0.17%
greater than actual.
This error is significantly less than the 2,0% error assumed
by
PP&L in the FSAR and subsequent
Core Operating Limit Report transient analyses.
The inspector discussed
the potential generic aspect of the conversion factor, and
the results of PP5L's design basis effort for CTP, with the NRR Project Manager and
Technical Staff. This issue is under consideration for generic applicability and
communication to the industry.
The violation of the CTP limit is further discussed
in Section 08.2 of this report
under LER 50-387,388/96-17.
Conclusions
A conversion constant affecting the reactor water cleanup system flow value used
to calculate the average core thermal power was not correct.
The condition is
thought to have existed since initial startup of both Susquehanna
units and resulted
in the indicated CTP being one mega-watt thermal greater than actual.
This error is
considered to be of low safety consequence
when compared to the licensed CTP of
3441 MW~, even when combined with other CTP calculational problems identified
in the last two years.
Stora
e of Transient
E ui ment Located Near Safet
Related
E ui ment
Ins ection Sco
e 71707
During the performance of a plant tour the inspector identified a 4.16 kV circuit
breaker that was stored outside of a designated
area in a Unit 1, 4.16 kV
switchgear room.
The circuit breaker had its wheels locked but was next to the
switchgear and could have impacted it if the breaker fell over.
b.
Observations
and Findin s
The Shift Supervisor was notified of the breaker placement issue and it was
immediately removed.
The inspector determined that the breaker storage.was
not
in compliance with licensee procedure NDAP-QA-0552, Transient Equipment
Controls, in that it was not in an approved
area and it was within a topple distance
of the distribution board.
In NRC Inspection Report 387,388/96-10, Section 02.3, Transient Material Storage
in the Unit 1 and 2 Reactor Buildings, the storage of material in designated
areas
was inspected.
The areas identified in NDAP-QA-0552 were originally supported
with an engineering evaluation and an expectation of what type of material was to
be stored in each of the areas.
However, the licensee had failed to carefully control
the types of material placed in these areas.
In this case, the breaker was stored
outside of approved storage areas.
C.
Conclusions
The licensee failed to control the placement of equipment near safety related
equipment (4.16 kV switchgear) in accordance with plant procedures.
Ad 'quate
corrective actions were undertaken
by the licensee after the issue was identified to
them.
This constitutes
a violation of minor consequence
and is being treated as a
non-cited violation consistent with Section IV of the NRC Enforcement Policy.
03
Operations Procedures
and Documentation
03.1
Postin
of Notices to Workers 71707
Notices to workers required by '10 CFR 19.11 were inspected to determine whether
the required information was appropriately and conspicuously
posted.
The inspector observed the NRC required postings at the North and South
Gatehouses,
and the Control Structure access.
The required information was found
to be appropriately posted, including a notice describing where documents not
practicable to post may be examined.
07
Quality Assurance
In Operations
07.1
Review of Third Part
Audits 71707
The inspector reviewed two Institute of Nuclear Power Operations
(INPO) reports, in
the offices of PP&L, that described conclusions from the SSES Plant Evaluation
conducted
in July 1996 and the Technical Training Program Accreditation
performed in September
1996.
No additional NRC regional followup is required
other than the routine planned inspection of the licensee's corrective action program
(CR process).
08
Miscellaneous Operations Issues (92700)
08.1
Control Rod Scram Accumulator Alarm
NRC Inspection Report 50-387,388/96-11,
Section 0.4, addressed
the actions of
operators
in response to the loss of all scram accumulator alarms and the
applicability of TS 3.1.3.5 and TS 3.1.3.1.
TS 3.1.3.1 included an "otherwise"
clause which directed certain activities be taken by the operators.
The inspector
determined that the "otherwise clause" was applicable to the plant condition.
The
NRC inspection report states that:
"The inspector determined that the otherwise clause of TS 3.1.3.1 Action b.1
would be applicable and directed operators to insert the inoperable withdrawn
control rods and disarm the associated
directional control valves.
This action was
not implemented by the operators."
To prevent an improper interpretation of the above paragraph,
it would have been
more clear to have stated:
"The inspector determined that the 'otherwise clause'f TS 3.1.3.1 Action b.1
would be applicable.
This TS directs operators to insert the inoperable withdrawn
control rods and disarm the associated
directional control valves.
These TS required
actions had not been implemented by the operators."
At no time did the inspector direct the actions of licensed operators.
08.2
Closed
LER 50-387 96-17: Non-Conservatism
in Heat Balance Calculation
On December 3, 1996, PP&L identified that a conversion constant used to
determine the mass flow rate for Reactor Water Cleanup system flow in the reactor
heat balance calculation was incorrect.
Consequently,
the indicated CTP was lower
than the actual value by approximately 1.0 MW~. As reported by PP&L in the LER,
it is likely that at some time both SSES units exceeded
their licensed CTP limit when
averaged
over an eight hour shift (reference August 22, 1980 Memorandum from E.
L. Jordan,
Discussion of Licensed Power Level). As discussed
in Section 02.1 of
this report, exceeding the licensed CTP by
1 MW~ (or -0.03/o of the original
licensed CTP) is a licensee identified and corrected violation and is being treated as
a non-cited violation consistent with Section VII.B1 of the NRC Enforcement Policy.
08.3
Closed
IFI 50-387 94-19-01: Licensee's Abilit to Activate the Backu
Emer enc
0 cretin
Facilit
The purpose of this IFI was to evaluate the ability of the licensee to establish
a
backup EOF near Hazleton, PA. Subsequent
to this IFI being written, the licensee
established
an EOF at the East Mountain Business Center near Wilkes-Barre, PA.
The establishment of this new facility eliminated the need to ensure that the backup
EOF was functional.
The new EOF was activated and performed adequately during
the July 1996 emergency exercise.
This issue is closed.
08.4
Closed
IFI 50-387 95-16-01: Emer enc
Pre
aredness
Trainin
The purpose of this IFI was to evaluate the licensee's training of emergency
preparedness
personnel
in a computer program (MIDAS). The inspector verified that
training was completed prior to the 1996 full-scale emergency exercise and the
skills acquired during the training were adequately demonstrated
during the 1996
emergency exercise.
This issue is closed.
I
08.5
Closed
LER 50-387 96-10: Main Steam Line Penetration
Leaka
e Rate Exceeded
Technical S ecification Limit
With Unit 1 shutdown on September
15, 1996, PP&L identified that the "as found"
leakage through both inboard and outboard main steam isolation valves exceeded
the requirements
of TS 3.6.1.2c.
The licensee further determined that the off site
dose rate using "realistic assumptions" for a loss of coolant accident would be
below the current licensing basis analysis.
The inspector reviewed the data discussed
in the LER and identified no problems
additional to the one that the licensee reported under 10 CFR 50.73.
As such, the
issue, identified and properly reported by the licensee, was a failure to meet NRC
requirements.
Adequate corrective actions were undertaken
by the licensee when
the issue was identified by them.
This constitutes
a licensee identified and
corrected violation and is being treated as a non-cited violation consistent with
Section VII.B.1 of the NRC Enforcement Policy.
08.6
Closed
LER 50-387 96-11: Secondar
Containment
B
ass Leaka
e Rate
Exceeded Technical S ecification Limit
With Unit 1 shutdown on September
18, 1996, PPSL identified that the "as found"
leakage through both inboard and outboard high pressure coolant injection
containment isolation valves exceeded
the design basis requirements of 9.0
standard cubic feet per hour.
The licensee further determined that the off site dose
rate using "realistic assumptions" for a loss of coolant accident would be below the
current licensing basis analysis.
The inspector reviewed the data discussed
in the LER and identified no problems
additional to the one that the li'censee reported under 10 CFR 50.73 and the current
secondary containment bypass leakage licensing issue being analyzed by NRC under
a Task Action. As such, the issue identified and properly reported by the licensee
was a failure to meet NRC requirements.
Adequate corrective actions were
undertaken
by the licensee when the issue was identified by them.
This constitutes
a licensee identified and corrected violation and is being treated as a non-cited
violation consistent with Section VII.B.1 of the NRC Enforcement Policy.
10
08.7
Closed
LER 50-387 96-12: Missed Firewatch
With Unit
1 shutdown on September
15, 1996, PP&L identified that the
compensatory
fire watch required by TS 3.7.7, was not established for fire
zone 1-5B.
The inspector reviewed the corrective actions performed by the licensee which
included training and counseling of personnel
and a limited analysis of the impact of
the missed firewatch.
The impact of the missed firewatch was determined
by the
inspector to be of minor consequence
and the corrective actions were determined to
be adequate.
The issue, identified and properly reported by the licensee, was a
failure to meet NRC requirements.
Therefore, it constitutes
a licensee identified and
corrected violation and is being treated as a non-cited violation consistent with
Section VII.B.1 of the NRC Enforcement Policy.
08.8
U date
LER 50-387 96-13: Reactor Condition Chan
e
During the Unit 1 startup on October 18, 1996, a mode change to Condition 2
(Startup) was made without the 'B'oop of the Residual Heat Removal s'stem being
operable for its Low Pressure
Coolant Injection (LPCI) function.
Both LPCI
subsystems
are required to be operable
in Condition 2 by TS 3.5.1.
This condition
was identified by the licensee and corrected within 44 minutes of taking the mode
switch to the Startup position.
The inspector reviewed the corrective actions performed by the licensee, which
included training and counseling of personnel
and system realignment, for
immediate safety impact.
The licensee's immediate corrective actions were
determined to be adequate.
The issue was identified and properly reported by the
licensee,
and it was a failure to meet NRC requirements.
This issue will be
reviewed further to determine its safety significance and will remain open.
08.9
U date
LER 50-388 96-09: 'O'HR Pum
Failure To Start
On November 21, 1996, with Unit 2 in Condition 1, the 'D'HR pump failed to
start when it was aligned for suppression
pool cooling.
The cause of the start
failure was determined to be a limit switch for the pump's suction valve that did not
provide the RHR logic a full open indication.
The lack of open indication from the
suction valve (i.e., no suction path) results in an RHR pump trip. PPBcL had
determined that the limit switch problem occurred on November 14, 1996, and
TS 3.5.1 Action b.1 allows a seven day outage time for one RHR pump.
However,
PPRL was not aware the pump was inoperable until November 21 when the
problem was identified and corrected.
Immediate licensee actions to verify operability of the all RHR pumps on both Units
were reviewed by the inspector and found to be thorough.
This issue will be
reviewed further to determine its safety significance and will remain open.
11
II. IVlaintenance
NI1
Conduct of Maintenance
M1 ~ 1
Review Observation of Maintenance Activities
a.
Ins ection Sco
e 62707
A review/inspection of the following maintenance
activities was performed,
including an evaluation of the return to service condition of the equipment.
In
.
addition, a sample of'the equipment permits (tagouts), drawings, and procedures
were evaluated.
., WA P61355
SLC 3-Year Preventive Maintenance for Pump 2P208A
WA V60315 Investigation of Breaker 2A203-04 Control Circuit Ground,
December 13, 1996.
RCIC Drain Pot Flushing, December 6, 1996.
WA P62210
RHR 1A Service Water Pump Discharge Check Valve Repair
WA P61008
RHR 1A Service Water Motor Doble Test
WA V66783
HPCI Cables
WA V63734 Graphite Packing
b.
Observations
and Conclusions
The inspector determined by observing/reviewing the above listed maintenance
activities and interviewing maintenance
personnel that the activity were performed
in accordance with the licensee's procedures
and regulatory requirements, that
personnel were appropriately trained and qualified, and that appropriate radiological
controls were followed.
M1.2
Surveillance Test Activit Sam
le Reviews
aO
Ins ection Sco
e 61726
The following selected surveillance tests were reviewed to ensure that TS
requirements were met, test equipment was calibrated, test data was accurately
recorded and complete, and that the system was adequately
returned to service.
SO 259-011
Suppression
Pool Level and Temperature,
Unit 2
SO 024-001
'A'mergency Diesel Monthly
SO 024-001
'C'mergency
Diesel Monthly
'A'REOASS charcoal and HEPA Bypass Testing,
December 18, 1996
Sl-254-001
Rod Exercising, Unit 2
SE-104-103, Degraded
Grid
12
b.
Observations
and Conclusions
The inspector determined that testing was accomplished
by qualified personnel
in
accordance
with approved test procedures.
Test results met TS requirements
and
any test discrepancies
were rectified.
M1.3
Review of On oin
and or Emer ent Maintenance Activities - Unit 1 H dro en
Ox
en Anal zer
a.
Ins ection Sco
e 62707
A review/inspection of corrective maintenance
associated
with the Unit 1 Hydrogen/
Oxygen analyzer was performed.
b.
Observations
and Findin s
The inspector performed
a walkdown of a portion of the system, and
reviewed/inspected
the following material associated
with the corrective
maintenance
conducted between October 17 and 24, 1996:
WA V66750, H,$0, Analyzer
WA S67431, H,>0, Analyzer
NDAP-QA-502, Work Authorization System
IOM 522, Instrument and Operations Manual, Comsip Hydrogen/Oxygen
Analyzer
In addition, the inspector discussed
the maintenance
activities with SSES
maintenance
personnel,
reviewed the need for permits (tagouts) and evaluated the
vendor technical manual for impact on the design basis functions associated with
selected components
of the analyzer.
The corrective maintenance
was conducted
as minor maintenance,
in accordance
with SSES procedure MT-AD-509-1, Minor
Maintenance.
'
The inspector determined that the documentation
included in the indicated WA
packages
did not include acceptance
criteria for calibration response,
acceptance
criteria for gas volumetric flow rates, or an operability determination to account for
as-found gas flow rates lower than the manufacturer expected value.
In one
instance TS related Channel Check, SO-100-002, was performed and in the other
instance it was not.
In neither case was the instrument calibration performed
following corrective maintenance.
The inspector was not able to determine from
the documentation
alone what criteria was used by the Operations Shift Supervisor
to determine the operability of the
Unit 1 Hydrogen/Oxygen
Analyzer upon return
to service.
The inspector discussed
the subject maintenance
activities with Maintenance
Department first line supervision,
and the Nuclear System Engineering and
determined that the actual maintenance
was adequately performed and that the
13
C.
equipment was operable.
It was not possible to determine operability of the
equipment without the supporting discussions
with the SSES personnel.
. ~
Conclusions
Hydrogen/Oxygen
analyzer maintenance
activities did not completely document the
as-left condition of the equipment.
Therefore, it was not possible to determine post
maintenance
operability of the equipment without supporting discussions with the
SSES maintenance
and NSE personnel.
The failure to adequately document the
performance of safety related maintenance
and the basis of equipment operability
constitutes
a violation of minor consequence
and is being treated as a non-cited
violation consistent with Section IV of the NRC Enforcement Policy. This issue is
closed.
M1.4 Observation of Ma'or Surveillance Testin
- HPCI Quarterl
Flow Surveillance
80
Ins ection Sco
e 61726
Portions of two performances of surveillance SO-252-002,
HPCI Quarterly Flow
~ Surveillance, were observed/reviewed
to determine compliance with TS
requirements,
verify proper licensee review/approval, evaluate the adequacy of
equipment permits (tagouts), verify the adequacy of operating system and test
instrumentation,
and verify the restoration of the portions of the HPCI system to
serwce.
b.
Observations
and Findin s
SO-252-002 was performed on the HPCI system twice during this inspection period.
On the initial performance of the surveillance,
a short loud, noise resulted.
The
noise was heard at the HPCI pump station and in the control room.
The noise
resulted from a water hammer in the HPCI normal injection line and the HPCI test
recirculation line. The water hammer resulted from a mis-coordination of steps
6.4.12 and 6.4.13 of the procedure.
Step 6.4.12 initiates HPCI and step 6A.13
has the operator open the HPCI test line to the condensate
storage tank by opening
isolation valve HV-255-F011.
The intent of step 6A.13 was to open the test line at
an appropriate time in order to prevent piping draindown, and at the same time, to
prevent the differential pressure
on the test isolation. valve from exceeding that
which the valve operator could overcome.
The impact of the water hammer on the operability of the system was evaluated by
the inspector.
Folio(wing discussions with the NSE system engineer and a review of
CR-96-2203, CR-96-1364, inservice testing results, periodic testing results,
previous water hammer incidents, and a detailed equipment walkdown performed by
the licensee, the inspector determined that the water hammer incident that occurred
during this inspection period had no identified impact on HPCI operability.
14
c.
Conclusions
During one of the performances
of SO-252-002,
HPCI, Quarterly Flow Surveillance,
a short loud, noise resulted from a water hammer.
The water hammer was caused
by the test configuration but also impacted the injection line. The impact of the
water hammer on the operability of the system was determined to be non-
consequential
in nature and the licensee took adequate
corrective action to prevent
further HPCI water hammer events.
No violation of NRC requirements was
identified.
I
M1.5
Review of Preventive Maintenance
Backlo
The inspector performed
a review for outstanding work authorizations
(WAs) to
assess
whether the backlog of safety related preventive maintenance
is being
appropriately managed
by PP&L.
b.
Observations
and Findin s
On November 25, 1996, the inspector requested
a printout of the preventive
maintenance
WAs that had reached
PP&Ls "violation" date (i.e., scheduled
due date
plus 25% grace period).
There were no WAs found in this overdue category.
The inspector also examined
a listing of WAs that were waived and therefore
deferred until their next regularly scheduled
occurrence.
In all cases examined, the
waived PMs were due to an adjustment in schedule
based
on past performance
and
the cognizant licensee personnel were able to provide reasonable
background
information.
On January
10, 1997, the inspector discussed
Maintenance
Supervision.
The licensee has a plan in place to eliminate the backlog
of 135 activities by March 1997, and has determined that no PMs required for the
environmental qualification of safety related equipment are in the existing backlog.
The inspector reviewed a sample of items from a computer printout of PM backlog
and did not identify any examples of maintenance
activities affecting equipment
environmental qualification.
C.
Conclusion
PP&L has a preventive maintenance
backlog reduction plan in place that is being
monitored by SSES Plant Management.
Based on a sample review of the backlog,
the inspector independently verified the licensee's determination that no overdue
activities affect the environmental qualification of the equipment.
15
M1.6
Unit 2 Standb
Li uid Control Pum
Dischar
a.
Ins ection Sco
e 71707
During a plant tour the inspector identified that the Unit 2, 'A'tandby liquid control
(SBLC) pump accumulator (2T207A) appeared
to have been replaced, because it
was a different size than the SLBC Unit 2, 'B'ump
The inspector
pursued what appeared to be an undocumented
modification of a safety related
system.
b.
Observations
and Findin s
Following discussions with the licensee, the inspector determined that the
accumulator on the A pump was not the one identified in drawing SP-DCB-201-6
nor was it supported
by seismic calculation SR-2877.
Although the capacity of the
modified accumulator met the original design capacity, the modified accumulator
differed from the original in weight (67 pounds vice 187 pounds)
and
shape.
The licensee wrote CR 96-2233 in response to this issue and performed an
The licensee concluded that the stresses
for the modified
accumulator were less that 30 percent of the SLC system allowable stresses
and
therefore do not impact the operability of the SLC system.
The licensee was not able to precisely determine under what process or at what
time during or since construction the accumulator had been replaced.
However, it
is believed to have been
a construction error.
The failure to control the replacement of safety related equipment in accordance
with plant procedures
constitutes
a violation of minor consequence
and is being
treated as a non-cited violation consistent with Section IV of the NRC Enforcement
Policy. This issue is closed.
C.
Conclusions
An undocumented
replacement of a Unit 2 standby liquid control pump accumulator
was identified by the inspector.
The licensee's
response to the technical issue was
quick and complete.
The safety impact of the identified replacement was low
because the capacity of the accumulator met its system design requirements.
M1.7
Effectiveness of Licensee Controls for Maintenance
a.
Ins ection Sco
e 62707
The inspector reviewed HPCI on line maintenance
activities to assess
the
effectiveness of corrective actions for previously identified issues regarding the
operability of HELB protective features.
16
b.
Observations
and Findin s
NRC Inspection Report 50-387/96-08 discussed
a finding from June 19, 1996,
regarding the operability of RCIC room HELB protective features when barriers, such
as doors or floor plugs, are blocked opened during power operation.
Unresolved
item (URI) 387, 388/96-08-06 was opened pending
a PP&L engineering evaluation
to assess
this configuration relative to the plant's design basis and to determine its
safety significance.
The report also discussed
a finding that the corrective actions
from the June '19 CR were not adequate to prevent a similar finding with a Unit 1
reactor water cleanup room on July 10, 1996.
During the HPCI on line maintenance
conducted
during the week of December 9,
the licensee again failed to provide adequate
control over a HPCI room door that is
assumed to be closed by the HELB analysis.
Altl>ough the significance of the
missing HELB room barrier has not yet been evaluated
by PP&L, the failure to
control the condition in the interim is considered
ineffective corrective action.
PP&L's failure to provide adequate
control to prevent the two recurrences
of
blocked open HELB room doors, after being identified by the corrective action
process,
is considered
a violation of 10 CFR 50 Appendix B, Criterion XVI,
"Corrective Action." (VIO 50-387, 388/96-13-01)
C.
Conclusions
PP&L's repeated failure to provide adequate
control for high energy line break room
doors, blocked open in support of maintenance,
is considered
a violation of
10 CFR 50 Appendix B, Criterion XVI, "Corrective Action." The ability of the plant
to meet its design basis in this configuration is still under review and is being
tracked by NRC unresolved item URI 50-387/96-08-06.
M1.8
Effectiveness of Licensee Controls for Maintenance
aO
Ins ection Sco
e 62707
The inspector observed
a portion of the performance of Standby Gas Treatment
System (SGTS) maintenance,
WA S60439, MT-GE-038 Hydrometer Overhaul
~
b.
Observations
and Findin s
During the performance of this maintenance,
power was removed from the 07553A
damper actuator under red tag permit 1961264.
Following changeout of the
damper actuator, the maintenance
technicians energized the actuator inside a
blocking permit boundary in order to stroke the actuator.
SSES NDAP-QA-322,
Permit and Tag, implements the tagging process at SSES.
Section 5.5 of NDAP-
QA-322 defines a foreign potential as an energy source applied within the boundary
of a blocked out system.
Section 6.2.3 states that the system operating
(SO)
representative,
system permit supervisor and all sign-ons shall be notified by the
person performing a foreign potential test and give their approval prior to application
of the foreign potential.
It further states that proper documentation
shall be noted
0
17
on the Permit Status Change Log, form NDAP-QA-0322-6. TS 6.8.1 requires that
written procedures
shall be established
and implemented for applicable procedures
recommended
in Appendix 'A'fRegulatory Guide 1.33, Revision 2, February
1978.
Regulatory Guide 1.33 requires procedures for the control of maintenance
repair and replacement of safety related equipment including a method for obtaining
permission and clearance for operations personnel to work, and for logging such
work. Contrary to the NDAP requirements,
110 Vac power (a foreign potential)
was brought inside the permit boundary without the proper approvals, or
documentation.
(VIO 50-387, 388/96-13-02)
No personnel
injury or equipment damage occurred as a result of the procedural
violation. The licensee issued
CR 96-2095 to affect corrective actions for the
above stated issue.
c.
Conclusions
During the performance of standby gas treatment system maintenance,
power was
returned inside a blocking permit boundary without meeting the requirements of the
licensee's tagging and permit procedure.
Although no personnel injury or equipment
damage occurred, this is considered
a violation of TS 6.8.1.
M2
Maintenance and Material Condition of Facilities
M2.1
Maintenance
and Material Condition of Facilities
During this inspection period, Unit 1 equipment experienced
several minor incidents
of transient behavior.
These included vibrations on a recirculation pump, reactor
water level spikes, and voltage oscillations on the main generator exciter.
Operators responded
well to the incidents, initial corrective actions were adequately
initiated and licensee management
established
good root cause
and diagnostic
actions.
Maintenance activities were adequately performed and the long term
availability of the equipment in each case was restored;
M3
Maintenance Procedures
and Documentation
M3.1
Unit 2 Reactor Buildin
Elevation 766 Access 0 enin
a.
Ins ection Sco
e 62707
During a plant tour the inspector identified an access
opening that was cut into the
grating above residual heat removal (RHR) containment spray (CS) vent valve
251029.
b.
Observations
and Findin s
The inspector determined that there was an approximately 18" square hole in the
grating, that was covered with a removable plate.
Based on licensee provided
information the opening and plate do not appear on the platform and grating
18
drawings for the valve access
area and as such constitute an undocumented
modification.
In addition, adjacent grating locations did not possess
the proper hold
down clips and studs.
The licensee conducted
a safety impact review (MFP-QA-2200), reinstalled the
missing grating clips under WA V63836, and documented
the condition in CR 96-
2268. Activities as a result of the CR identified two additional grating modifications
of the same sort identified by the inspector.
The conclusion of the nuclear safety impact sheet was that the grating was not
safety related, would not affect safety related equipment and even though the
modifications were not documented,
they met the current SSES seismic two over
one requirements,
C.
Conclusions
The licensee's
response to the undocumented
modification of grating near safety
related equipment was adequate.
PP&L determined that there was no safety impact
resulting from the modification.
The inspector agreed that because
the modification
was on nonsafety related equipment and was determined to meet the licensee's
current seismic two over one process, there was no impact on safety related
equipment.
M8
Miscellaneous Maintenance Issues (92902)
IVI8.1
Closed
Violation 50-387 96-10-02 Control Rod Drive Mechanism
Re lacement
a.
Ins ection Sco
e 62707
A review of the licensee's corrective actions and root cause evaluation for the
above stated violation was performed by the inspector.
b.
Observations
and Findin s
The licensee responded to the above stated violation in a letter (Byram/Pasciak)
dated December 17, 1996.
In that response
the licensee identified a clerical error in
the violation which identified the cited procedure
as MT-055-001 vice the correct
MT-055-015. The error was not substantive
and the licensee's
response,
and
corrective actions were adequate.
The licensee's root cause evaluation was
aggressive
and insightful in that it identified a number of subtle contributions to the
event, was quick in its evaluation of the event, involved a large cross section of
SSES technical expertise and was subjected to the routine high standards
of the
19
C.
Conclusions
The failure to perform an adequate
control rod drive mechanism replacement was
adequately
responded to and corrected by the licensee.
The licensee's root cause
evaluation was aggressive
and insightful. This violation is closed.
III. En ineerin
E1
Conduct of Engineering
E1.1
En ineerin
Problem Resolution
a.
Ins ection Sco
e 37551
The inspector reviewed a selection of approximately 40 CR issues which involved
the resolution of engineering related problems and/or incidents.
b.
Observations
and Conclusions
The inspector determined that the licensee adequately identified the root causes of
the selected engineering problems, during this inspection period.
The licensee
implemented an effective process of identifying, resolving, and preventing problems.
In addition the aggressive,
questioning efforts of PORC strengthened
the area of
engineering
and the performance of safety related systems.
E3
Engineering Procedures
and Documentation
E3.1
Unit 2 Standb
Li uid Control Pum
Dischar
e Flow Desi
n Basis
a.
Ins ection Sco
e 37551
During a plant tour the inspector observed that the Unit 2, SLC pump flow
calibrations use pure water as a medium, which discharges through a recirculation
flow path.
The scope of this inspection was to evaluate whether or not the water
remaining in the SLC injection line at the completion of the surveillance test was
accounted for in the design basis of the plant.
b.
Observations
and Findin s
The inspector reviewed the following engineering
design documents:
Calculation EC-ATWS-0505, SABRE Computer Code for Simulation of Boiling
Water Reactor Dynamics Under Failure to Scram Conditions.
Calculation EC-ATWS-1001, Calculation of Unit 2 cycle 9 Peak Suppression
Pool Temperature for ATWS Conditions.
'
20
GE Proprietary Report GENE-637-024-0893,
Evaluation of Susquehanna
ATWS Performance for Power Uprate Conditions.
Note: This document was
returned to the licensee upon the completion of the review.
The calculations assume
a delay of approximately 95 seconds for operator action
(injection initiation), and a 30 second delay from the initiation of boron injection to
the time that boron enters the core.
The 30 second delay accounts for actuation
times of switch positions, motor starting, squib valve actuation, and a volume of
unborated water to be discharged
into the core prior to the boron injection.
The
calculations appear to be conservative
and represent the delay in boron injection
accurately.
C.
Conclusions
Standby liquid control pump flow calibrations use unborated water as a medium and
discharge through a recirculation flow path. At the completion of the test the
normal discharge/injection flow path into the vessel is left filled with unborated
water.
The licensee was able to produce design basis documentation that takes
into account a 30 second delay from the time of boron initiation to the time that
boron actually enters the core.
These calculations conservatively account for the
unborated water left in the injection line following the surveillance flow testing.
This issue is closed.
E3.2
Re Iacement Item Evaluation
RIE
a.
Ins ection Sco
e 37551
During a plant tour the inspector observed the replacement of an ITT General
Controls NH-90 Series model b Hydrometer actuator.
The replacement involved the
use of an improved model b-1 actuator, of a slightly different design.
The new
model was accepted
under the SSES RIE program.
The adequacy of the actuator
replacement under this program was reviewed by the inspector.
b.
Observations
and Findin s
The inspector reviewed the following engineering design documents:
Environmental Qualification (EQ) Assessment
Report - EQ Binder EQAR-074
ITT General Controls Report 730.1.140
ITT Barton Confidential System Engineering Report, R3-EQ-16.
Note: This
report was treated as a proprietary item and returned to the licensee
following its review.
NP-QA-301, Preparation of Replacement
Item Evaluations
21
Based on a'review of the documents
listed above, and a field inspection, the
inspector agreed with PP5L's conclusion that'the form, fit and function of the
replacement
ITT actuators were consistent with the original component design
requirements.
C.
Conclusions
The replacement of ITT General Controls 90 model b Series Hydrometer actuators
with an improved model b-1 series of a slightly different design was adequately
addressed
by the licensee's
RIE program.
E8
Miscellaneous Engineering Issues (92902, 2515/109)
E8.1
Review of the U dated Final Safet
Anal sis Re ort UFSAR
A recent discovery of a licensee operating their facility in a manner contrary to the
Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a
special focused review that compares plant practices, procedures
and/or parameters
to the UFSAR descriptions.
The inspectors compared the MOV design assumptions
for the Reactor Core Isolation Cooling (RCIC) steam isolation valve (HV-249F007),
and the Reactor Water Cleanup (RWCU) system isolation valve (HV-244F001) to
design parameters
contained in the susquehanna
Engineering study VALV-
0508 assessed
how elevated ambient temperatures
Section 6.2.3 of the Susquehanna
UFSAR contained the drywell and suppression
pool peak accident temperatures
and pressures.
The inspector verified the design
calculations considered
in EC-VALV-0508 for valves HV-249F007 and HV244F001
were identical to the drywell peak accident temperature
limits listed in section 6.2.3
of the Susquehanna
PPS.L had appropriately incorporated the temperature
design parameters
contained in the UFSAR when developing MOV design
assumptions
for valves HV-249F007 and HV-244F001.
While performing the
inspections discussed
in Section E3.1 of this report, the inspectors reviewed the
applicable portions of the UFSAR. The inspectors verified that the UFSAR wording
was consistent with the observed plant practices, procedures
and/or parameters.
E8.2
Closed
URI 50-388 95-20-01: Standby Liquid Control IST Instrumentation
This item was opened pending the results of a rotameter flow Instrument
calibration/investigation
and PPRL's final evaluation regarding the method of
calibration for ultrasonic flow transducers.
The vendor calibration of both rotameters involved in a prior failed surveillance were
found to be within 1% accuracy.
During further investigation by PPSL, including
discussion with the rotameter vendor, it was identified that the PPRL installation
procedure did not follow the vendor's installation instruction to null the rotameter
after installation.
Based on review of the test results, and this new information,
PPSL concluded that the failure to null the rotameter was the most probable cause
of the apparent flow degradation
on July 25, 1995.
22
Since this occurrence,
PP&L has had the ultrasonic flow transducers
for each Unit's
SLC system calibrated by the vendor on a flow loop.
The inspector noted that
calibration of this type is consistent with industry practice (reference
Response
5.5-7),
PP&L does not currently plan to perform periodic calibration of
the ultrasonic transducers
since the rotameter flow instrument will be used for
inservice testing in the future.
The failure to provide adequate
procedures for installation and calibration of the test
device for SLC flow (rotameter) led to erroneous
indication during a surveillance test
required by TS. This failure to provide adequate
procedures for control of
measuring
and test equipment constitutes
a violation of minor consequence
and is
being treated as a Non-Cited Violation consistent with Section IV of the NRC
URI 50-388/95-20-01
is closed.
E8.3
U date
Unresolved Item 50-387 94-14-01
50-388 94-15-01:
pressure
locking
and thermal binding of gate valves.
The inspectors reviewed the status of PP&L's program for assessing
the
susceptibility of motor-operated
gate valves to pressure
locking or thermal binding
(PLTB). Generic Letter 95-07, "Pressure Locking/Thermal Binding of Safety-Relateo
Power-Operated
Gate Valves," requested
the licensee to identify safety-related
power-operated
gate valves that may be susceptible to PLTB phenomena
and take
appropriate compensatory
actions.
In a February 13, 1996, submittal to the NRC,
PP&L identified eighteen valves that were susceptible to PLTB. PP&L indicated that
the corrective actions for the 18 valves, which may be susceptible to pressure
locking, are scheduled to be completed before the startup following the Unit 2 8th
refueling outage, which is presently scheduled for April 1997.
PP&L had performed
an operability determination on the valves and concluded they were operable.
In a
letter dated June 10, 1996, the NRC asked PP&L to supply additional information
concerning its submittal.
The inspectors reviewed PP&L's February 13, 1996,
submittal and did not find any immediate safety or operability concerns regarding
the eighteen valves.
However, this item remains open pending NRR review of the
February 13, 1996, PP&L pressure locking analysis.
E8A
Motor-Operated Valve Program Review
E8.4.1
Motor-0 crated Valve Pro ram Review
On June 28, 1989, the NRC issued Generic Letter (GL) 89-10, "Safety-Related
Motor-Operated Valve Testing and Surveillance," requesting
licensees to establish
a
program to ensure that switch settings for safety-related
motor-operated
valves
(MOVs) were selected, set, and maintained properly.
Seven supplements to the GL
have been issued to clarify the NRC request.
NRC inspections of Pennsylvania
Power and Light's (PP&L's) actions have been conducted
based on guidance
contained
in NRC Temporary Instruction (Tl) 2515/109, "Inspection Requirements
for Generic Letter 89-10."
23
On February 2, 1996, PP&L notified the NRC that the GL 89-10 program was
complete.
The purpose of the current (fourth) inspection was to perform a closeout
review of the Susquehanna
Steam and Electric Station (SSES) GL 89-10 program.
The NRC had previously conducted the initial Part
1 program inspection at SSES in
September
1991, as documented
in Inspection Report (IR) 91-80.
A followup
inspection
(IR 93-08) was performed in August 1993 to assess
how SSES had
addressed
the issues identified in the Part
1 inspection.
During October 1994, the
NRC performed
a Part 2 inspection at the PP&L corporate office as documented
in
IR 94-14/15.
As outlined in the following sections of this report, the inspectors concluded
had used inadequate
methodologies to account for the effects of load sensitive
behavior (LSB) and establishing valve factors for some untested valves.
However,
based upon a review of valve design margin, test results and MOV guidance
documents
and procedures,
the inspectors concluded MOV switch settings were
acceptable.
Therefore, PP&L had implemented
a program that met the intent of
Generic Letter 89-10 "Safety-Related Motor-Operated Valve Testing and
Surveillance."
S
E8A.2
Summa
Status of Generic Letter 89-10 Motor-0 crated Valves
The inspectors reviewed procedures, test data, and design guides which
documented
PP&L's GL 89-10 program at SSES.
There are 206 MOVs in the
program.
PP&L verified the design margins of 39 valves by performing dynamic
tests under differential pressure
(DP) conditions with diagnostic equipment.
used the dynamic test results to establish the logic settings for 21 butterfly and-
Using dynamic test results obtained from in-plant testing and tests
performed by the Electric Power Research Institute (EPRI), PP&L established
control
logic settings for 42 Anchor Darling gate valves.
PP&L verified the design margins of 32 valves by using the EPRI MOV Performance
Prediction IVlodel (PPM) software.
The control logic settings of 58 valves were
found acceptable
by PP&L based upon excess design margin, or their location in low
DP systems or flow assist-to-close
applications.
Fourteen valves had recently been
added to the MOV program.
PP&L ensured the design margins of those valves were
adequate
by grouping them with valves tested under dynamic or static conditions.
PP&L's methods for demonstrating
MOV design-basis
capability included:
1)
valve-'pecific
dynamic tests at, or near, design-basis
conditions; 2) valve-specific tests,
linearly extrapolated to design-basis
conditions; 3) valve grouping; 4) valves with
little or no DP requirement deemed capable based
on available margin; 5) valves
deemed
capable based
on available or excess margin or in flow-assist-to-close
applications;
6) statistical analysis and application of EPRI and in-plant test data;
and 7) use of the EPRI MOV PPM software model.
To review the seven analysis methodologies,
one valve out of each group was
selected for review. The inspectors reviewed test results and engineering
'valuations
in detail for the following MOVs:
24
HV-1 56F059
HV-1 55F002
HV-1 55F003
HV-1 51 F004
HV-1 49F007
HV-143F031A
HV-1 1 21 OA
HPCI Lube Oil Cooler Supply Valve
HPCI Steam Supply Inboard Containment
Isolation
HPCI Steam Supply Outboard Containment Isolation
RHR Suppression
Pool Suction
RCIC Steam Supply Inboard Containment Isolation
Recirculation System Discharge valve
Service Water Supply to RHR
E8.4.2.1
MOV Sizin
and Switch Settin
s
aO
Ins ection Sco
e
The inspectors reviewed the following: Engineering Calculation Valve (EC VALV)
study 1020, "SSES MOV Program Design Philosophy Study," study EC-VALV-
1008, "Combination of Inaccuracies,
Repeatabilities,
and Margins Associated with
MOV Diagnostic Testing,"
Mechanical Design Standard
(MDS) 04, "Design
Standard
For Motor-Operated Valve Program Engineering Requirements,"
and MDS-
06, "Design Standard
For Verification of Motor-Operated Valve Functionality."
The
inspectors focused upon how PP&L developed
and controlled MOV sizing and
control logic switch settings.
Design Standards
MDS-04 and MDS-06 outline the methodology used to evaluate
the ability of an MOV to function under design-basis
conditions, as well as the
process
used to establish the required MOV switch settings.
The methodologies
outlined in MDS-04 and MDS-06 were based upon a series of studies, that PP&L had
conducted
on MOVs. Studies EC-VALV-1008 and EC-VALV-1020 strongly
influenced the development of PP&L's MOV sizing and switch setting process.
b.
Observations
and Findin s
PP&L used the standard industry equations for MOV sizing and switch settings.
For
gate and globe valves with a safety-related
close function, the torque switch is
bypassed
for 97% of valve stroke.
The torque switch for butterfly valves with a
safety-related
close function is bypassed for 100% of valve travel.
PP&L assumed
a stem friction coefficient of 0.15 to convert torque to thrust when establishing the
initial closing thrust values for Anchor Darling valves.
For other valve types, and
when calculating the required opening thrust for Anchor Darling valves, a stem
friction coefficient of 0.20 was used.
During the initial MOV control logic switch setup,
a valve factor of 0.50 was used
for gate valves and 1.1 for globe valves.
The MOV program required adjustment of
the valve factors and the minimum required thrust if the results of in-situ testing
dictated that a larger value was required.
When establishing the initial MOV switch
settings for gate and globe valves with a safety function to close, PP&L
incorporated
a 10 percent design margin (DM) into the minimum required static
thrust/torque criteria. The DM was intended to account for the effects of load
sensitive behavior, stem lubricant, and valve seat degradation.
25
Following dynamic testing, if the 10% DM did not bound the observed
LSB effects,
a new DM was calculated that would bound LSB.
For gate and globe valves that
were not dynamically tested,
PPSL ensured the DM thrust bounded
LSB and other
uncertainties
including equipment errors, such as torque switch repeatability and
diagnostic system accuracies.
PPSL combined these errors in a "square root sum-
of-the-squares"
(SRSS) methodology to develop
a minimum required thrust.
If the
DM thrust did not bound the errors, a new value was calculated.
The inspectors
~ concluded that this treatment of LSB as a random error was incorrect, however, for
the reasons
outlined in Section E8.4.2.3, the error was not significant.
Some MOVs
were classified as marginal (i.e., less than 10% DM), and became candidates for
increased monitoring or modification.
1
For gate and globe valves with an open safety function, PPSL did not provide a
specified DM to account for LSB effects or valve degradation.
However, PPRL did
adjust the open thrust limitto account for diagnostic system error.
The lack of a
LSB margin in the open direction was not significant since the valves had adequate
margin.
For butterfly valves, allowances for torque switch repeatability and.diagnostic
system errors were applied directly to the minimum required closing torque.
A 10%
DM was then added to the minimum required torque to account for seat
degradation.
C.
Conclusions
PPSL appropriately considered the effects of torque switch repeatability and
diagnostic s'stem inaccuracy.
Additionally, GL 89-10 MOV's were demonstrated
to
have adequate
margin.
However, as outlined in the following sections of this
report, the methods used inadequate
assumptions to develop valve factors for some
valves and to account for the effects of LSB.
E8.4.2.2 'alve Factor and Grou in
aO
Ins ection Sco
e
The inspectors reviewed MOV guidance documents
MDS-04 and MDS-06, and
engineering study EC-VALV-0535 "Motor-Operated Valve Program Valve Factor
Justification" to determine how PPRL developed the valve factors and grouping
.
methodologies
used in the MOV program.
The inspectors also reviewed engineering
study.EC-VALV-1054, "Documentation of the Basis for the Use of the Statistical
Approach for Evaluating the Functionality of Certain Non-Testable
which compared the methodology PPSL had used to develop valve factors for non-
dynamically tested Anchor Darling valves to methodologies that were more
commonly used in the nuclear industry.
A
26
Observations
and Findin s
PP&L had placed valves that were not dynamically tested into six categories for
analysis purposes.
These categories were based upon the following criteria:
1)
valve manufacturer;
2) application; 3) similarity to valves that had received dynamic
tests; 4) excess design margin; 5) valves that used the EPRI'PPM software program;
and 6) valves in flow-assist-to-close
applications.
PP&L considered
only the valves
that were categorized
based upon their similarity to valves that had received
a
dynamic test as "grouped" valves per the criteria of GL 89-10 supplement
6.
Valves Grou
ed b
Manufacturer
PP&L had placed 42 Anchor-Darling flex-wedge gate valves in one group.
The valve
switch settings were originally established
using a valve factor of 0.5. To validate
the valve factors, PP&L performed an analysis of dynamic test results conducted at
PP&L selected valves from the EPRI test program based upon their
similarity, (e.g., same size, type, flow conditions) to SSES valves.
Based on their review of the data for valves that had an open safety function, PP&L
used a valve factor (approximately 0.6) which encompassed
95% of the test data.
For valves that had a close safety function, PP&L established
the required thrust by
using the mean valve factor value and combining the random valve factor term with
allowances for torque switch repeatability, LSB and other terms using a SRSS
methodology.
PP&L assumed
a design margin of 17.01% to account for LSB. If >he
calculated thrust exceeded the initial set up thrust required by the 0.5 valve factor,
the valve switch settings were placed at the new value.
PP&L did not decrease
any
thrust settings below a 0.5 valve factor.
The EPRI data did not represent
a statistically valid test program because
only a few
MOV's of various type and manufacture were tested; also, some valves were not
preconditioned
and revealed low thrust requirements that are not reliable for plant-
specific requirements.
Therefore, the inspectors did not agree with the PP&L
statistical approach to valve factor calculation or the methodology used to develop
a
required valve thrust.
In response,
PP&L calculated "available" valve factors based
upon the "as-measured"
thrust requirements.
PP&L outlined the results in study
EC-VALV-1054. PP&L's data indicated the majority of the valves had adequate
margin with available valve factors greater than 0.6. Two valves that had valve
factors'less than 0.6 had already been identified as marginal by PP&L and were
subject to increased monitoring.
The inspectors reviewed the SSES test data and independently
performed a
statistical analysis resulting in a valve factor of 0.501 at the 95% confidence level
for the close direction.
Using PP&L's assumptions for LSB and torque switch
repeatability, the inspectors calculated
a required thrust for a sample of four gate
valves (HV-155F006, HV-15766, HV-21313, and HV-251F004).
This
independently
calculated thrust was then compared to the present MOV switch
setting, and ultimately found to be adequate.
Although the method PP&L'used to
develop the valve factors for Anchor Darling gate valves was not acceptable,
the
27
inspectors
did not identify any operability concerns.
Therefore, based upon the
available margin for the Anchor Darling valves, the inspectors considered the valve
switch settings to be acceptable.
Valves Grou ed b
A
lication
Twenty-four gate valves in 0 psid applications were grouped together.
The valve
switch settings were set up during static testing based
on a valve factor of 0.50
and an added design margin of 10%.
The 10% margin was used to accommodate
LSB effects and valve degradation.
The inspectors performed
a qualitative review of the valve switch settings and
grouping methodology.
Based upon the low DP and large valve factors, the
inspectors determined the grouping and valve switch settings were acceptable.
Valves Grou ed b
Similarit to D namicall
Tested Valves
Gate and Globe Valves
PPSL had four gate and five globe valves which were grouped with other
dynamically tested valves.
Two of the four gate valves were grouped with other in-
plant tested valves (four valves total in the group).
Two of the five globe valves
were grouped with other in-plant tested valves (four valves total in the group).
However, the remaining five valves were not grouped per the recommendations
of
GL 89-10, Supplement
6. Specifically, the three globe valves were placed in groups
of two with only one SSES valve tested per group.
The remaining two gate valves
were grouped using an EPRI tested valve.
The inspectors reviewed the switch settings and grouping methodology for the gate
and globe valves.
The inspectors determined the switch settings for the valves
(grouped per the recommendations
of GL 89-10, Supplement
6) were adequate.
However, since only one valve was tested in some groups, the inspectors could not
determine if the tested valve's performance characteristics
represented
the group
population.
Despite the minimal test data, the inspectors noted the switch settings
for the grouped valves appeared to have adequate
design margin.
Butterfl
Valves
PPSL had six groups of butterfly valves.
One group consisted of four Posi-Seal
valves which had a design-basis
DP of zero psid.
A second group consisted of four
Contromatic valves where two of the four valves were dynamically tested using
diagnostic equipment.
There were four groups of Jamesbury butterfly valves which
consisted of one group of eight valves and three groups with two valves in each
group.
Only one valve in each group of the Jamesbury butterfly valves'had
been
dynamically tested using diagnostic equipment.
The remaining valves in the groups
had received dynamic tests'without diagnostics.
The valve switch settings were
established with a design margin of 10% to account for valve seat degradation.
28
Butterfly valve diagnostic testing revealed that the vendor-recommended
switch
settings were not conservative; therefore, PP&L established
settings based upon
their own diagnostic test results.
The PP&L methodology for establishing switch
settings for Contromatic valves was based upon sound statistical analysis in that
two valves per group were diagnostically tested.
The inspectors reviewed the
switch settings for'these valves and determined they were acceptable.
Due to the lack of Jamesbury
diagnostic test data, the inspectors were concerned
about the reliability of the switch settings for those valves.
Specifically, since only
one valve per group was tested,
PP&L could not determine if the tested valves
performance ch'aracteristics
adequately
represented
the valve population. However,
the inspectors noted that the Jamesbury
valves had considerable
available margin,
and as part of the GL 96-05 periodic verification effort, the licensee will be
expected to~validate its torque requirement predictions.
Valves Grou ed b
Desi
n Mar in
PP&L had placed 32 MOVs, (12 gate valves and 20 globe valves), in one group
based upon excess design margin.
The gate valves switch settings were
established
using a valve factor of 1.0.
The switch settings for the globe valves
used
a valve factor of 2.0.
PP&L assumed
a 10% design margin to account for
load sensitive behavior.
Most of the 32 MOVs in this group had thrust margins of
at least 100%; therefore, the inspectors considered the valve switch settings in this
group acceptable.
PP&L analyzed 32 MOVs using the EPRI Performance
Prediction Model (PPM)
software program.
For non-blowdown valves, PP&L assumed
a 17% design margin
for LSB. For valves in systems that may be subject to blowdown conditions, PP&L
assumed
a design margin of 8%.
PP&L had reviewed the NRC's safety evaluation report (SER) on the PPM, and used
the software according to the EPRI manuals and the NRC SER with two notable
exceptions.
First, PP&L had used the program on four 28-inch Lunkenheimer
recirculation system discharge gate valves.
validated using Lunkenheimer valves.
Therefore, the software may not accurately
predict the performance of these valves.
PP&L stated the EPRI PPM program was
.
used on the Lunkenheimer valves since the valves could not easily be dynamically
tested and industry test data was not available.
The required thrust predicted by the EPRI PPM for the Lunkenheimer valves was
equivalent to using a valve factor of 0.6 with a design basis DP of 200 psid.
The
inspectors noted the SSES Lunkenheimer valve factor was comparable to the
assumptions
the industry had used for similar large bore gate valves.
Because
no
SSES or indust'ry Lunkenheimer dynamic test data was available from which
adequate
comparison could be drawn, the inspectors determined PP&L's alternative
approach for the Lunkenheimer valves acceptable
on an interim basis.
However,
29
since these valves were outside the scope of the EPRI PPM, the licensee will be
expected to validate its thrust predictions as industry information becomes
available.
ll
Second, when the EPRI PPM was run on several valves in the Residual Heat
Removal (RHR), Reactor Water Cleanup (RWCU), and High Pressure
Coolant
Injection (HPCI) systems, the EPRI PPM reported the valve thrust as
"unpredictable."
However, PPSL still used estimated thrust numbers predicted by
the EPRI PPM to verify the valves were operable.
The inspectors reviewed the
calculations for two of the valves in the HPCI system (HV-155F002 and HV-
155F003) for which the EPRI PPM program predicted unpredictable thrust
requirements.
Since PPSL was not aware of internal valve measurements,
worst
case valve dimensions were used, and the program was unable to accurately predict
a required valve thrust during portions of the valve stroke.
To obtain the necessary
internal dimensions,
PPtkL had developed
plans to disassemble
the low margin
valves in the HPCI system and measure
and modify, specific internal dimensions.
Although the EPRI program could not accurately predict the required valve thrust
throughout the range of the valve stroke, the PPM program did produce estimated
thrust in ".he "unpredictable" region.
PPRL considered the valves operable since the
MOVs produced considerably greater thrust than the EPRI program had predicted.
PPSL calculated available valve factors for the twelve valves that EPRI PPM had
determined were "unpredictable."
The valve factors ranged from 0.9 to 1.0 at
seating, and greater in the flow region where DP was lower.
At the time of the inspection, Unit 1 was in a refueling outage and PPSL was
obtaining the required measurements
for valves in the Unit 1 HPCI system.
PP5L
indicated similar measurements
would be performed on the Unit 2 valves during an
upcoming refuel outage.
To reduce radiation exposure,
PP&L indicated the valves in
the RWCU system on both units would not be disassembled
for the sole purpose of
obtaining data to run the EPRI PPM program.
PPS.L however stated that, if
subsequent
industry testing revealed the current setup to be not conservative, they
would reevaluate their course of action.
The inspectors considered
PPSL's actions concerning the valves identified as
unpredictable to be acceptable
(in the short term), based upon the high available
valve factors and the fact that the valve torque switches are bypassed
during 97%
of the valve's stroke.
However, ALARAshould not be used as a sole basis for
deferring actions to address
a potential safety concern.
Flow-Assist-to-Close Valves
SSES had four globe valves which were in applications wherein flow assisted
in
closing.
The valves were grouped in accordance
with the criteria outlined in
Supplement
6. The inspectors reviewed the valve thrust calculations
and the grouping criteria and determined the valve grouping, torque switch settings
and thrust margins were adequate.
30
C.
Conclusions
PP&L's mhthodology for developing valve factors for untested Anchor Darling
valves was not acceptable.
However, based upon the current valve switch
settings,'the
inspectors agreed with the licensee's conclusion that the valves had
design basis capability.
The inspectors noted PP&L was in the process of
evaluating industry information (e.g., EPRI guidelines for LSB assumptions)
for
inclusion into the SSES MOV program to ensure potentially non-conservative
assumptions
were removed.
E8.4.2.3
'Load-Sensitive
Behavior
a.
Ins ection Sco
e
Load sensitive behavior (LSB) is a change
in MOV output thrust due to a change
in
internal friction forces under dynamic conditions.
The inspectors reviewed the
following MOV studies to assess
how PP&L accounted for LSB: EC-VALV-0538,
"MOV Rate of Loading," EC-VALV-1008, "Combination of Inaccuracies,
Repeatabilities,
and Margins Associated with MOV Diagnostic Testing," and EC-
VALV-1025, "Determine Acceptability of Current Use of Design Margin to Account
for Rate of Loading and Determine Appropriate Value of Design Margin to be Used
for Non-Testable MOVs."
b.
Observations
and Findin s
To account for the effects of LSB, PP&L used data obtained from in-situ
Susquehanna
tests as well as industry tests performed by EPRI.
The data was
separated
by valve type and analyzed statistically to establish upper and lower
limits. The gate valve analysis consisted of 28 valves with a sample mean of
0.92% and a 95% confidence interval that 90% of the data was between -15.16%
and 17.01%.
Based upon the statistical analysis, PP&L used 17.01% as an
assumed
value for LSB for gate valves.
PP&L determined that an analysis of the globe valve data could not be performed
since the sample size (7 MOVs) was too small. Although LSB for the seven globe
valves ranged from -17.8% to 31.8%, PP&L assumed
a 25% margin to account for
the effects of LSB was acceptable.
This margin was based upon an evaluation of
test results performed on similar valves in the industry.
PP&L accounted for the effects of LSB by combining the LSB assumption with other
variables such as torque switch repeatability and diagnostic system errors in a SRSS
methodology.
These errors were converted into a design margin (DM) multiplier,
=
and applied to all non-testable
MOVs to adjust the required thrust in the closed
direction.
The inspectors
had three concerns regarding PP&L's assumptions
which tend to
underpredict
LSB:
31
1.
Eleven data points were obtained from the EPRI test program but, the
environmental test conditions may not be identical to those at SSES;
2.
When developing
a margin to account for LSB, PP&L considered
LSB effects
to be a random variable that could be combined with other errors such as
torque switch repeatability and diagnostic system error.
The NRC position is
that industry test data has shown that LSB is caused
by an increase
in stem
friction under dynamic conditions and that most valves exhibit some LSB.
Therefore, LSB is considered
as a bias or bias)random
error rather than pure
random error; and
3.
PP&L did not include a DM to account for LSB for valves that had a safety
function to open.
LSB could reduce thrust in the open direction.
Using the SSES dynamic test results and treating LSB as a biased rather than
random error, the inspectors recalculated the thrust requirements for gate valve
HV-151F004D, since it had low margin.
The predicted thrust requirement was then
compared to the PP&L calculated numbers to determine if original (viz. random) LSB
assumptions
were bounded by the test data.
Assuming the mean value (3.9%) was
a bias error, and the upper confidence limit was a random error, the inspectors then
independently
recalculated the thrust for valve HV-151F004D using a valve factor
of .62. the predicted thrust was less than the PP&L predicted values, therefore, the
assumption was conservative for this valve.
c.
Conclusions
Although PP&L's methodology for calculating LSB was inconsistent with the general
understanding
of the phenomenon,
an acceptable
margin accounted for the effects
of LSB when establishing switch settings.
Although PP&L did not assume
a specific
value for LSB in the open direction, the SSES MOV program required valves to have
a DM, based on motor capability, of at least 10 percent.
MOVs that had less than
10 percent margin required increased monitoring or modification.
The inspectors
concluded the MOVs had sufficient DM to accommodate
the effects of LSB in the
open direction.
E8.4.2.4
Stem Friction Coefficient
a e
Ins ection Sco
e
The inspectors reviewed MOV guidance documents
MDS-04, MDS-06, and
engineering studies EC-VALV-0536 "MOVStem to Stem-Nut Coefficient of Friction"
and EC-VALV-1007, "Evaluation of Motor Capability and Maximum Allowable Open
Thrust for GL 89-10 MOVs Assuming a Stem/Stem Nut Coefficient of Friction of
0.20," to determine how initial MOV stem friction coefficient assumptions
were
established.
32
To assess
how stem friction coefficient test results were used to determine MOV
design margin, the inspectors reviewed engineering study EC-VALV-1022, "Generic Letter 89-10 Periodic Verification Method Evaluation."
b.
Observations
and Findin s
PP&L assumed
a stem friction coefficient of 0.15 to convert torque to thrust when
establishing the initial closing thrust values for Anchor Darling valves.
For other
valve types, and when calculating the required opening thrust for Anchor Darling
valves,
a stem friction coefficient of 0.20 was used.
PP&L did not provide an
allowance for changes
in the stem friction coefficient due to lubricant
degradation'ince
tests conducted
between 18-month operating cycles revealed lubricant
degradation
did not occur.
EC-VALV-0536 contained the results of stem, friction coefficients measured
during
in-situ plant testing..The test results confirmed the 0.20 stem friction coefficient
assumption was conservative.
Specifically, a PP&L statistical analysis of measured
stem- to-stem nut coefficients of friction for SSES MOVs indicated
a mean of 0.12
for static conditions with a 95% confidence range of 0.05 to 0.18.
Dynamic test
results revealed
a mean of 0.13 with a 9" % confidence range of 0.07 to 0.18.
Although the test data revealed the initial 0.15 stem friction assumption was not
conservative for some Anchor Darling MOVS, PP&L's methodology for calculating
MOV design margin ensured non-conservative
changes
in stem friction coefficient
were evaluated.
Specifically, when MOV design margins were calculated, PP&L
used the stem friction coefficient measured
during dynamic testing.
If an MOV did
not receive a dynamic test, PP&L used the static stem friction coefficient measured
during testing with an additional bias to account for load sensitive behavior.
that had less than a 10% design margin required modification or increased
monitoring.
C.
Conclusions
PP&L's test data confirmed the validity of the assumed
stem friction coefficients.
E8.4.2.5
Linear Extra olation.
a 0
Ins ection Sco
e
The inspectors reviewed PP&L's methodology for extrapolating test data contained
in engineering study EC-VALV-1023, "Justification for Linear Extrapolation of
Thrust."
b.
Observations
and Findin s
PP&L required MOV dynamic tests to be performed at a minimum of 50% of design-
basis DP before linearly extrapolating test data.
The inspectors reviewed test data
33
and found the lowest case in which results were extrapolated was from 79% of
normal operating pressure
(valve HV-250F045).
Although the SSES extrapolations were performed at large DPs, the inspectors did
not find a requirement in SSES's
MOV procedures that outlined a minimum DP
below which no extrapolation was valid (e.g., 50 psi).
Industry experience
has
shown extrapolating test results at low DPs may produce nonconservative
test
results because
of data scatter at low pressures.
PP&L corrected this deficiency by
revising their MOV program during the inspection to require MOV engineers to
review the DP to be extrapolated for appropriateness.
The inspectors considered
this change acceptable.
c.
Conclusions
The inspectors considered
PP&L's methodology of linear extrapolation to design-
basis conditions acceptable.
E8.4.2.6
D namicall
Tested Valves
a.
Ins ection Sco
e
The inspectors reviewed MOV guidance document MDS-06, maintenance
procedures
M-1503, "Verifying Motor Operated Valves Abilityto Function,"
MT-EO-021, "Votes - MOV Diagnostic Test," valve matrix sheets containing open
and close valve limitations and margins, and diagnostic test documents for the
selected MOVs.
b.
Observations
and Findin s
PP&L had 206 IVIOVs in their program of which 39 MOVs were dynamically tested
using diagnostics.
This amounted to 19% of the MOV population receiving a
dynamic test.
Since PP&L did not utilize industry test data from other plants, a
significant amount of statistical analysis was performed to verify MOV design basis
capabilities.
The analysis methodology was discussed
in section E8.4.2.2 of this
report.
PP&L used Liberty Technologies'OTES
diagnostic equipment to test their MOVs.
The inspectors reviewed test data from MOVs that had received dynamic tests, and
verified PP&L had applied the diagnostic system inaccuracies to their MOV settings
when determining MOV thrust requirements.
c.
Conclusions
The inspectors considered
PP&L's verification of design-basis
capability for MOVs
that were dynamically tested to be adequate.
34
E8.4.2.7
Trackin
and Trendin
aO
Ins ection Sco
e
Item (h) of GL 89-10 requested
licensees to establish,
in part, a monitoring and
feedback effort to establish trends in MOV operability.
The inspectors interviewed
SSES MOV personnel to determine how PP&L tracked and trended MOV
performance.
PP&L described the tracking and trending process
in NDAP-QA-0017,
"Motor-Operated Valve Program."
The inspectors reviewed 15 condition reports
(CRs) that reported MOV deficiencies to evaluate the PP&L corrective actions.
b.
Observations
and Findin s
PP&L had established
a substantial amount of MOV performance data.
The data
bases were in the process of being consolidated
into one program, entitled the
Nuclear Information Management
System (NIMS) data base.
PP&L tracked several
MOV parameters
including thrust, torque and stem factor.
Once each operating
cycle, maintenance
technology was tasked with reviewing MOV performance.
The
review required analyzing the information contained
in the data bases to identify
MOV degradation
and the need for additional testing or maintenance.
The inspectors reviewed the MOV data bases
and concluded the information would
be useful to assess
MOV performance changes.
The inspectors noted PP&L had
already used the information to diagnose
MOV performance deficiencies.
The
inspectors performed a summary review of CRs that documented
MOV performance
deficiencies.
The inspectors verified each deficiency had been evaluated for
reportability and operability.
C.
Conclusions
PP&L had developed
an adequate
trending program.
The program systematically
trended valve failures and provided a method to detect degrading MOV
performance.
MOV performance deficiencies had been adequately documented
via
the CR system.
E8.4.2.8
Periodic Verification
Ins ection Sco
e
The inspectors interviewed personnel
assigned to the MOV Program regarding "as-
found" testing of MOVs to assess
how PP&L willtrack potential degradation of
stem lubrication and changes
in valve factor.
Further, the inspectors reviewed the
periodic verification program guidance document Mechanical Design Standard
(MDS) procedure 08, "Periodic Performance Assessment
of SSES Motor-Operated
Valves" and study EC-VALV-1022 "Generic Letter 89-10 Periodic Verification
Method Evaluation" to assess
how PP&L will monitor MOV performance.
35
Observations
and Findin s
MDS-08 was the guidance document that outlined the responsibilities of the
engineering department concerning the MOV periodic verification program.
Contained in the document were the MOV performance characteristics that should
be monitored, how they should be monitored, and how changes
in MOV
performance should be assessed.
To monitor the performance of gate and globe
valves, PPRL will perform static and dynamic tests with diagnostic equipment.
Butterfly valves would primarily receive dynamic tests without diagnostic
equipment.
MDS-08 required variations in MOV performance characteristics
be documented
in
an annual report.
Performance characteristics that would be monitored included
changes
in stem factor, motor capability margin, and torque in the close direction.
The criteria used to determine the test frequency for rising stem valves included
percent excess motor capability, risk significance, potential for aging and thrust
margin.
Based upon the criteria, a rising stem valve could receive a retest at 2, 5 or
10-year intervals.
Currently, PPS.L intends to perform dynamic tests with
diagnostics
on six gate and globe valves.
PPSL was revising the MOV program
procedures to ensure the periodic diagnostic tests are performed before preventive
maintenance
activities.
These "as found tests" would ensure
PPRL could detect
changes
in valve performance that occurred between preventive maintenance
intervals.
PPSL had scheduled
dynamic tests for four butterfly valves with diagnostics for a 5-
year period.
The remaining butterfly valves would receive dynamic tests without
diagnostic equipment.
PPSL selected the four butterfly valves for dynamic
diagnostic testing based,
in part, on the potential for those valves to be
overstressed
because
of torque switch degradation.
As discussed
in sections E8.4.2.2 and EBA.2.3 of this report, PP5L had performed
only limited diagnostic testing of butterfly valves and did not provide an allowance
for stem lubricant degradation.
The inspectors noted PPSL's periodic verification
program would validate the basis for those assumptions.
Conclusions
The PPS.L periodic verification program will be reviewed in greater detail as part of
PPSL's response to GL 96-05.
Desi
n Modification Process
and Im lementation
Ins ection Sco
e 37550
The scope of this inspection was focused on:
(1) the design modification process,
(2) engineering involvement in the resolution of technical issues,
and (3) the
36
Susquehanna
snubber reduction program.
The inspectors reviewed and verified the
implementation of procedures for engineering design modifications.
Observations
The Desi
n Modification Process
The licensee conducted
Individual Plant Examination for External Events
(IPEEE)
walkdowns to ensure compliance with seismic qualification requirements
and to
identify vulnerabilities for the plant.
During these walkdowns, the licensee noted
excessive
gaps between adjacent cabinets/panels
that were not fastened together.
This condition was noted at several locations in the control room and in the upper
and lower relay rooms.
The NRC inspector reviewed the corrective action which consisted of joining these
cabinets/panels
to adjacent cabinet/panels
through bolting. This corrective action
was implemented through modification package
Nos. DCP-95-9047 and -9048.
The
shop drawings in the package illustrating the details of the connections
were clear
and had sufficient detail for assembly.
The package was prepared
in accordance
with design procedures.
Another Modification No. 95-3014F installed condensate
supply and return piping
associated
with the condensate
filtration project.
The inspectors verified that the
provision of ANSI B31.1 were met by performing the prescribed inservice leak test
(ISLT). In addition, the licensee performed nondestructive
examination; however,
the package stated that the provisions of ASME Section IX Code Case N-416-1 =in
conjunction with the supplemental
requirements
per NRC safety evaluation for relief
request
RRPT-1 be met.
This statement was incorrect since the design basis for
this piping system was not ASME Section III, Class 3 piping.
The licensee reviewed
other packages to ensure that this error was not generic.
PPS,L subsequently
determined the error was an isolated case.
En ineerin
Involvement with the Resolution of Technical Issues
When reviewing DCP-95-9047 and 9048, the inspectors noted the licensee did not
perform an operability determination that had addressed
the acceptability of the
current plant configuration.
In response to the inspector's observation, the licensee
performed an operability determination.
The inspectors reviewed the operability determination and noted the licensee had
previously developed
a detailed finite element seismic analysis model of the
cabinet/panels.
The licensee model of the maximum safe shutdown earthquake
(SSE) displacements
of the cabinet/panels
due to front-to-back and side-to-side
excitation, concluded very low displacements.
These low displacements
yielded
low dynamic impact loads on the cabinets/panels
enclosures,
and to the safety-
related components
within. Therefore, the panels were operable based upon their
as-found condition.
0
37
Sus
uehanna
Snubber Reduction Pro ram
Susquehanna
Steam Electric Station (SSES) Units
1 and 2 utilize mechanical
as seismic and dynamic supports of nuclear piping systems.
Operating
experience
on both units indicates the existence of snubber performance difficulties.
The licensee has initiated a snubber reduction and replacement program.
The
program aimed at eliminating the largest possible number of snubbers through pipe
stress analysis using the provisions of the American Society of Mechanical
Engineers
(ASME) Code,Section III, basic code cases, Welding Research
Council
(WRC) Bulletin 300, and by appropriate replacement with more reliable supports
(e.g. struts).
NRC Regulatory Guide 1.84, revision 24, accepted the basic code
cases used by this licensee in this application with certain conditions.
Since the
initiation of the snubber reduction program, the licensee has eliminated 1,618
snubbers from Unit 1 and 752 snubbers from Unit 2. At the close of the inspection
report period, there were 578 remaining snubbers
in Unit 1 and 487 in Unit 2.
The NRC inspector verified that ASME Code requirements were properly applied in
the snubber reduction program, including the fulfillment of the conditions stated in
the NRC Regulatory Guide 1.84, rev. 24.
Specifically, the inspector verified that
the stress analysis for the nuclear class
1 core spray (CS) piping from containment
penetration X-16A to the reactor pressurized
vessel (RPV) nozzle N-5A was
performed in accordance
with the rules of the code of record (Article NB-3600 of
the ASIVIE Section III Boiler and Pressure
Vessel Code 1977 Edition, summer 1979
addenda).
Conclusion
Design modification packages
were found to be complete and thorough.
Design
requirements were established
and documented
in the design modification package.
The responsible
engineers were cognizant of the pertinent regulatory requirements,
and compliance to the engineering procedures
was evident,
except for the error
found in package
No. 95-3014F which was promptly corrected.
The licensee implemented
an effective program that eliminated over 60 percent of
the mechanical snubbers
at the facility.
IV. Plant Su
ort
Radiological Protection and Chemistry (RP&C) Controls
Radiolo ical Controls
During routine tours of the plant the inspector verified that a sample of doors
required to be locked for the purpose of radiation protection, by Technical
Specifications and procedures,
were actually locked.
While touring the plant, the
inspector found that radiological areas were appropriately posted and that radiation
38
workers were following applicable Health Physics practices.
The ihspector also
found that the self contained breathing apparatus
(SCBA) units staged at various
locations in the plant indicated that periodic inspections
are being performed.
R6
RP8cC Organization and Administration
R6.1
Administrative Re uirements for Workers Involved in Safet
Related Activities
a.
Ins ection Sco
e 71707
The inspector verified that the licensee has a program intended to control the
regular use of overtime for workers involved in safety related activities.
Specifically, the process implemented to control health physics technician overtime
was reviewed.
b.
Observations
and Findin s
Overtime requirements
are established
by Unit 1, and 2, TS 6.2.2.
The SSES
site-wide program implementing these requirements
is described
in NDAP-QA-00-
0650, Conduct of Site Support.
The inspector selected the use of overtime by Health Physics
(HP) technicians
during the most recent 1996, Unit 1 refueling outage as a sample for this inspection
item.
Based on discussions with SSES HP management
and review of upper tier
documentation,
the inspector determined that there were approximately 60
instances where extended overtime was employed (greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in a 7 day
period) and that the HP Department did not have documented
practices in place to
control and limitthe routine use of overtime.
For the period covered by this
inspection sample, the licensee failed to meet the guidelines in TS 6.2.2 in limiting
the routine heavy use of overtime.
Following discussions with the inspector, the licensee initiated a condition report to
track resolution of the issue.
Prior to discussions with the inspector the Department
had identified the issue and established
the means to increase the number of
contract HP technicians for the upcoming Unit 2 refueling outage.
They also had
begun (in draft form) a program to control overtime in the HP Department,
HP-Hl-
083, Control of Overtime.
C.
Conclusions
The licensee failed to adequately control Health Physics technician overtime during
the most recent Unit 1 outage.
In approximately 60 cases the licensee did not meet
the guidelines in Technical Specification 6.2.2, "Unit Staff," which constitutes
a
licensee identified and corrected violation. This is being treated as a non-cited
violation consistent with Section VII.B.1 of the NRC Enforcement Policy.
39
V. Mana ement Meetin s
X1
Exit Meeting Summary
The inspectors presented
the inspection results to members of licensee management
at the conclusion of the inspection on January
13, 1996.
The licensee
acknowledged
and did not object to the findings as presented.
The inspectors determined that during the course of the inspection proprietary
materials were provided for the inspectors'eview.
These materials were discussed
in Sections 3.1 and 3.2 of this report in a way as to not disclose their proprietary
nature.
The materials were returned to the licensee after the inspectors completed
their review.
The licensee identified no other materials examined during the
inspection that should be considered
proprietary.
X3
Drop-in Meeting By PP&L Managers
Mr. W. Hecht and others of his staff, representing
PPRL management
conducted
a
drop-in meeting with NRC staff on November 14; 1996, at the Region
I office.
Representing
the NRC were Messrs.
H. Miller and A. Blough of the Region staff.
The topics covered during the meeting involved an overview of the PPRL
organization and the utility approach to Nuclear Department issues.
No conclusions
were formulated during the meeting.
Licensee briefing materials are attached to this
inspection report.
~Oened
50-387,388/96-1 3-01
50-387,388/96-1 3-02
Closed
ITEMS OPENED, CLOSED, AND DISCUSSED
Failure to provide adequate
control for HELB room doors
blocked open
Foreign Potential brought inside the permit boundary
without approvals, notifications or documentation
50-387/96-1 7
50-387/94-1 9-01
50-387/95-1 6-01
50-387/96-1 0
50-387/96-1
1
50-387/96-1 2
50-/387/96-1 0-02
50-388/95-20-01
LER
Non-Conservatism
in Heat Balance Calculation
IFI
Licensee's Abilityto Activate the Backup Emergency
Operating Facility (EOF)
IFI
Training
LER
Leakage Rate Exceeded
Technical Specification Limit
LER
Secondary Containment Bypass Leakage Rate Exceeded
Technical Specification Limit
LER
Missed Firewatch
Control Rod Drive Mechanism Replacement
Standby Liquid Control IST Instrumentation
Discussed
50-387 9/ 6-13
50-388/96-09
50-387/94-14-01
50-388/94-1 5-01
LER
Reactor Condition Change Without LPCI
LER
RHR Pump Failure To Start
Pressure
Locking/Thermal Binding
LIST OF ACRONYMS USED
CFR
CR
DR
ESS
IFI
LER
Mwi,
NRC
NSE
PCO
RP&C
Sl
TS
WA
Code of Federal Regulations
Condition Report
Control Room Emergency Outside Air Supply System
Core Thermal Power
Drain Recommendation
Emergency Operating Facility
Emergency Safeguard
System
Florida Power and Light
High Efficiency Particulate Air
High Pressure
Coolant Injection
Inspection Follow-Up Item
Institute of Nuclear Power Operations
Licensee Event Report
Mega-Watt Thermal
Non-Cited Violation
Nuclear Plant Operator
Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Nuclear System Engineering
Plant Control Operators
Plant Operations Review Committee
Reactor Core Isolation Cooling
Radiological Protection and Chemistry
Systematic Assessment
of Licensee Performance
Self Contained Breathing Apparatus
International System of Units
System Operator
Technical Specification
Updated Final Safety Analysis Report
Unresolved Item
Work Authorization
NRCRe ionI
Meetin wit
A rninistrator
PP8zL Senior Mana ement
Novernbez14, 1996
NRC Region I Offices
King ofPrussia, PA
~ Overview of PP8zL Resources
~ Key Corporate Issue
Electric.UtilityIndustry Restructuring
~ PP8zL's Approach to Nuclear
~ Key Nuclear Department Initiatives
~ Open Discussion
0
vervievr o
esources
CORPORATE STRUCTURE
"<<"-:"-=='-'"'PPP8IL!!RESQURCES-""-"'-"=:"='-'.s
'8~x:.>,'
"."A "~,"'~'~w.: '", '
'6'~PFg,
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':',,.'iiikki'i,ME@',i';::,'.COMPA'3'i:--:-:
-'.;:.-,",'-,',i'::SPECTRUM,,EIIIERG
,':NUCL'EAR'"DEPARTMENT'.:;
PP8zL Service Area Generation
WAL ENPAUPACK
Hyd
44
Generation
Coal
Nuclear
Oil/Gas
Hydro
Total Capacity
Customers
Residential/Business
Service Area
Average Revenue
Operating Revenues
Net Assets
Em lo ees
60%
34%
7.8 Mkw
1.2 Million
83% / 17%
10,000 sq. miles
7.1) / kwh
$2.8 Billion
$6.5 Billion
- 6,500
PP&I. DIMENSIONS
BRUNNER ISLAND
Coal
1469 MW
MA
NS CREEK
Coal,
1, Gas
1940 M
HOLTWOOD
Coal, Hydro
175 MW
MONTOUR
Coal,
- 1525MW-t,;;;,
V
",-*' SUSQUEHANNA
SUNBURY, '-: =."'.:.-'"" 1950 MW
Coal:<
-1950 MW
389 MW ..
4
vervievr 0
Corporate Strategic Direction
Superior Nuclear Performance
Focus on Core Business in the
Communities We Serve
Electric Energy Market Development
Shaping the Future for Competitive
Success
e
or orate
ssue
E ectric Utii
Industry Restructuring
Electric Utilities Have Made
Si
'cant Progress in the Transition
&omVertically-Integrated Franchised
Monopolies to Competitive
Businesses
e
or orate
ssue
E/ectric UtilityIndustry Restructuring
Safe Operation
>> Impacts of Business Decisions
Electrical System Reliability
>> Control of Transmission Facilities
Financial QualjLBcations
>> Funding Decommissioning
>> Definition of an Electric Utility
e
or orate
ssue
Electric UtilityIndustry Restructuring
~ PP &L'sPosition
. Comiinitment to Superior Nuclear Performance
Advocate for Competition
Heavy Involvement in Shaping Pennsylvania's
Model
>> Generation Reliability
>> Decommissioning-
>> Stranded Investment
>> PJM as an Independent System Opera'.or
roaC
to
uC ear
We Have a Conservative Operating Philosophy
Being Accountable for Safe Operation
Performing Self Assessments
and Maintaining an
External Perspective
Preserving Fundamentals While Continuously
Improving
Our Managemerit is Involved
Providing Active Leadership
Maintaining a Long Term Corporate Commitment
S
roac
to
uc ear
We Emphasize Communication
Listening to Others
Learning Through Industry Involvement
Fostering an Environment of Trust and Involvement With
Employees and the Public
We Maximize Employee Potential
Technical and Business Training
Developing Supervisors and Managers
We Plan for the Future
Safety, Reliability, and Financial Objectives are Mutually
Compatible
Key Nuclear Department Initiatives
~ October 9, 1996 NRC Letter
~ Employee Concerns Program
~ Supervisory Development
Key Nuclear Department Initiatives
October 9, 1996 10CFR50.54
Letter
Susquehanna
Current Licensing Basis Strengths:
>> Strong InitialReview and Documentation
>> Major Projects Aided Continued Enhancement
Proactive Assessment Began in February 1996
Enhancements
are Underway
Ongoing Work WillSupport a Thorough Response
Key Nuclear Department Initiatives
Employee Concerns Program
We Have Monitored the Effectiveness ofThis Program
Since Its Inception and WillContinue to Do So.
1995 ECP Periodic Independent Assessment
>> Strong Nuclear Safety Culture
>> Improved Sensitivity by Line Management
>> Employees/Contractors
are Willingto Raise Concerns
Periodic Independent Assessments WillContinue
Industry Lessons Learned
NRC Allegation Advisor Annual Report
Key Nuclear Department Initiatives
Supervisory Development
Leadership Academy
>> Designed to Enhance the Department's Ability
to Balance its Business, Interpersonal and
Technical 0'j~ectives
>> Modeled After Plant Certification Program
>> Focused Training on Management, Business
and Leadership Skills
15
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