ML17158B861

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Insp Repts 50-387/96-10 & 50-388/96-10 on 960910-1021. Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support
ML17158B861
Person / Time
Site: Susquehanna  
Issue date: 11/12/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17158B859 List:
References
50-387-96-10, 50-388-96-10, NUDOCS 9611190029
Download: ML17158B861 (48)


See also: IR 05000387/1996010

Text

0

TABLE OF CONTENTS (Continued)

IV. Plant Support............

R1

Radiological Protection and Chemistry (RP&.C) Controls..........

R1.1

ALARA.... ~ ..

R1.2

Control of Radioactive Material and Contamination ........

R1.3

External Exposure Controls........................

~

R1.4

Use of Flashing Lights for Access Control to High Radiation

Areas

%1

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R1.5

Response

to Alarming Dosimetry....................

~

R2

Status of RP&C Facilities and Equipment ....................

R5

Staff Training and Performance

in RP&C

R5.1

Staff Training

R6

RP&C Organization and Administration

R7

Quality Assurance

in RP&C Activities

R8

Miscellaneous

RP&C Issues

R8.1

Transverse

Incore Probe (TIP) Work ln December 1995.....

R8.2

Reactor Water Clean-up (RWCU) Pump Work ln January 1996

R8.3

(Closed) Violation 50-387;388/96-04-02 ....

~ . ~.......

~

R8.4

(Closed) Unresolved Item 50-387;388/96-09-02

R8.5

(Opened) Violation 50-387;388/96-10-03,

"Radiological

Posting Deficiencies" ..... ~....... ~....

~ ~........

~

S8

Miscellaneous Security and Safeguards

Issues ................

S8.1

(Update)

EA 95-250, Security Chilling Effect

(Update)

EA 94-212, Security Chilling Effect............

18

18

18

19

20

21

22

24

25

25

26

27

29

29

30

34

34

35

36

36

V. Management Meetings.................. ~.... ~......

~

~

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~

~

~

~ .

X1

UFSAR Review

X2

Exit Meeting Summary.... ~...... ~..................

36

36

37

VI

9biii90029 96iii2

PDR

ADOCK 05000387

8

PDR

Re ort Details

Summar

of Plant Status

Unit 1 began this inspection period in the refueling condition.

This condition was reached

on September

9, when the reactor head was detensioned.

Between October 19 and 20

the unit was restarted

and then returned to a shutdown condition in order to repair

acoustic flow indication equipment on the 'L'afety relief valve (SRV).

Unit 2 began this inspection period at 100% percent power.

With the exception of limited

decreases

in power, based on power control center (PCC) requests

and a period of

approximately one day at 80% power to support cooling tower chemistry limitations, the

unit operated throughout the period at 100% power.

I. 0 erations

02

Operational Status of Facilities and Equipment

02.1

Residual Heat Removal

RHR

S stem Ali nment

a.

Ins ection Sco

e 71707

Susquehanna

Steam Electric Station (SSES) routinely aligns the RHR System to send

post accident injection flow through the RHR heat exchanger

in parallel with the

RHR heat exchanger

bypass line.

b.

Observations

and Findin s

The system alignment was verified and reviewed by the inspector.

The Final Safety

Analysis Report (FSAR) is silent on the desired normal alignment.

It was determined

that the RHR heat exchangers

are designed to accept 10,000 gpm and site

operating procedures,

including emergency operating procedures,

limitthe flow

through the RHR heat exchangers to less than 10,000 gpm.

The practice of

aligning the RHR heat exchangers

in the normal injection path was determined to be

supported

by design basis calculations.

c.

Conclusion

In its normal 100% injection mode lineup, the RHR system is operated

in a

configuration that is consistent with the design basis and the design basis is

supported

by design basis calculations.

02.2

Unit 2 Turbine Combined Intermediate Valves

CIV

a.

Ins ection Sco

e 71707

The inspector reviewed a plant upset condition:

while testing the ¹3 CIV, the ¹1

CIV closed and then immediately opened over a 5 to 10 second period.

Observations

and Findin s

The operators responded

appropriately to the upset condition and the site

adequately

performed two operability determinations

in accordance

with the

guidance supplied in NRC Generic Letter 91-18.

The licensee initiated a corrective

action document,

CR 96-1680, and determined that the ability of the CIVs to

perform their intended turbine overspeed

protection design function was not

affected.

The inspectors reviewed operator actions and operator logs, discussed

the issue

with the operators

on shift at the time of the event, reviewed the operability

determinations

and evaluated the corrective actions,

The inspector determined that the ability of the turbine to be tested at power was

degraded

(note: this was in addition to a concurrent degraded

condition involving

the automatic voltage regulator).

However, the symptoms identified by the licensee

do not appear to impact the overspeed

protection function of the CIVs as the

symptoms are limited to test circuitry logic.

C.

Conclusion

OZ3

Operators adequately

responded to an unexpected

upset condition involving the

Unit 2 Turbine Combined Intermediate Valves.

Transient Material Stora

e in the Unit 1 and 2 Reactor Buildin s

Ins ection Sco

e 71707

SSES routinely stores transient material in assigned

areas within the Unit 1 and Unit

2 Reactor Buildings.

The inspector reviewed the process

used by the licensee to

control the material in these areas and inspected the material stored in the transient

areas to determine if there was the potential for an impact on the operation of

safety related equipment.

Observations

and Findin s

The licensee's

program for the control of transient material is addressed

in NDAP-

QA-552,Transient Equipment Controls.

The areas identified in this procedure were

originally supported with an engineering

evaluation and an expectation of what type

of material was to be stored in each of the areas.

The inspector viewed one area

near safety related high pressure coolout injection (HPCI) instrumentation at position

Q-29 in the Unit 2 reactor building.

When requested,

the licensee was able to

perform an engineering

evaluation (through Engineering Work Request M60310)

that the material presently stored in the area presented

no risk to the safety related

equipment.

However, the material that was actually placed in the storage

area was

not considered

in the original engineering

evaluation that was used to designate

the

area.

c.

Conclusions

Pennsylvania

Power 5 Light (PPSL) management

response to this issue was good

and identified no present impacts on the safe operation of plant equipment from the

storage of transient equipment.

The failure to fully control transient equipment near

'afety related equipment constitutes

a violation of minor significance and is being

treated as a Non-Cited Violation consistent with Section IV of the NRC Enforcement

Policy.

02.4

Unit 1

Restart between October 17 and 22

1996

Ins ection Sco

e 71707

The inspector reviewed the Unit 1 restart on October 22 which resulted in condition

1 operation at approximately 10:00 a.m.

The activities were well performed and

supervised.

Restart activities between October 17 and 18, 1996 resulted in the

Unit returning to condition 3 to repair the acoustic monitor associated

with the

'L'afety

relief valve.

During these earlier startup activities, several weaknesses

occurred which require further NRC inspection.

These weaknesses

are:

The operability of HPCI during the transient through 1504 psig in the RCS.

The operability of LPCI during the mode change into condition 2.

The operability of the acoustic monitors associated

with the A, G, L, and

R

SRVs.

The licensee's review and long term corrective actions for these weaknesses

have

not been completely characterized.

As a result, the NRC review of these

weaknesses

will be tracked under Unresolved Item, (URI 387/96-10-01).

04

Operator Knowledge and Performance

04.1

Control Room Emer enc

Outside Air su

I

S stem

CREOASS

Fan 'B'utlet

Dam er Failure

Ins ection Sco

e 71707

During a routine control room tour the inspector noted that the 'B'REOASS fan

outlet damper was not functioning properly.

The inspector reviewed the licensee's

initial and subsequent

actions for the degraded

safety-related

component,

the

applicable system technical specification (TS), and similar issues previously

identified by the NRC,

0

b.

Observations

and Findin s

Unit 1 TS 3.7.2 requires two subsystems

of CREOASS to be operable with the Unit

in Operational Condition 5. With one subsystem

inoperable, the inoperable

subsystem

must be restored to operable status within 7 days or the remaining

subsystem

must be placed in service.

NDAP-QA-0326, provides guidance for operations with the potential for draining the

reactor vessel (OPDRV). Attachment A of this procedure provides the requirements

for entering an OPDRV condition, including one that requires that certain Limiting

Conditions for Operation are met without reliance on Action St'atements.

Step 1.2

requires both CREOASS subsystems

to be operable, prior to entry into an OPDRV

condition.

SSES procedure

NDAP-QA-0702, Condition Report,

requires the identification,

reporting, evaluation and correction of conditions adverse to safety or quality. This

procedure

provides a mechanism for the types of corrective action required by 10

CFR Appendix B, Criterion XVI.

On September

22, the 'B'REOASS subsystem

was running in support of a

procedure to transfer the reactor protection system power supply.

When the

'B'REOASS

fan was shut down, its outlet damper (HD-07811B) remained open,

when it should have closed.

A NSE representative

was available at the time of the

failure and determined that the 'B'ubsystem was still operable.

A work

authorization was initiated to correct the condition.

However, no CR was initiated

and the basis for operability was not documented.

On September

24, control rod drive mechanism

(CRDM) replacement work began

which required the Unit Supervisor (US) to complete Attachment A of

NDAP-QA-0326 for the OPDRV.

On September

25, the inspector learned that CREOASS damper HD-07811B was

mechanically bound (failed) in the open position, contrary to the expected

as-

designed fail-closed position (shown in FSAR Figure 9.4-1).

The inspector noted

that there was no TS Action Statement entered in the LCO log for the 'B'REOASS

subsystem

due to the damper problem.

The inspector questioned

the US on shift

about his rational for operability of the 'B'REOASS subsystem.

The US stated

that he considered the damper operable because

it was in the position required for

the fan to function, but that the basis for this determination

had not been

documented.

The CRDM replacement work was placed on hold and the damper

was repaired prior to the CRDM work being allowed to restart.

On September

25, CR 96-1645 was issued to document the damper failure and an

operability determination.

The inspector found the justification provided by NSE a

reasonable

basis for operability.

Previous examples where the licensee failed to identify conditions adverse to quality

on safety-related ventilation system components

were documented

in NRC

Inspection Report 50-387/96-09.

5

The inspector concluded that the degraded safety related damper constituted

a

condition adverse to quality and that the licensee had not implemented their

corrective action process

in a timely manner.

The inspector also noted that changes

made to NDAP-QA-702, Revision 1, under PCAF 1-96-6510, deleted the examples

of conditions which warrant issuance

of a CR. Although this was not viewed as

justification for failure to implement the procedure, it may have caused some

confusion.

Conclusion

The licensee did not document an operability determination for a CREOASS damper

that had failed in an open position, despite the fact this position was contrary to its

fail-closed design.

Maintenance activities with the potential for draining the reactor

cavity were allowed to commence

based on the presumed operability of both

CREOASS subsystems.

The operability determination provided after questions from

the inspector provided a reasonable

basis for operability.

In this case, the failure to

implement required administrative procedures for a condition adverse to quality

constitutes

a violation of minor consequence

and is being t'reated as a Non-Cited

Violation consistent with Section IV of the NRC Enforcement Policy.

04.2

Nuclear Plant 0 erator Lo

Review

This section documents

NRC inspection activities of specific nuclear plant operator

(NPO) performance items.

The inspector interviewed several of the non-licensed

NPOs to determine the accuracy of certain operator round logs.

Of particular focus,

were those log items that required entries into high radiation areas to obtain specific

parameters.

the inspector reviewed several completed

NPO logs and interviewed

selected

NPOs.

No discrepancies

were identified relative to the adequacy

or validity

of the selected completed logs.

In addition, all NPOs interviewed were familiar with

the licensee's

requirements that prohibit individuals other than qualified NPOs from

obtaining required readings.

Based upon the log reviews and interview results, the

inspector concluded that the log readings for equipment located in high radiation

areas were properly performed by qualified NPOs.

06

Operations Organization and Administration

06.1

Overtime A

royal Review

Ins ection Sco

e 71707

The inspector reviewed the use of overtime by SSES staff who perform safety

related functions against the requirements of TS 6.2.2.f.

Observations

and Findin s

TS 6.2.2.f.2 provides guidance on the use of overtime hours and states that an

individual should not be permitted to work more than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in any seven day

period, excluding shift turnover.

SSES administrative procedure

NDAP-QA-0650

4

implements the TS requirements

and requires prior approval of deviation from the

overtime hour guidelines.

The inspector found that overtime limit deviation forms were completed in

accordance

with NDAP-QA-0650 and provided the required approval for several

licensed operators who exceeded

the limitfor 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> of work in 7 days during the

refueling outage.

The inspector reviewed a sample of licensed operator time

records and determined that the overtime limit deviation forms were being

generated

when required.

A sample of time records for workers in the Maintenance

Department was also

reviewed.

Three examples were identified where the prior approval for an overtime

deviation was not documented.

In response to the inspector's findings, the

Maintenance

Supervisor reviewed the refueling outage time records for the rest of

his organization and found no other examples.

The Maintenance

Supervisor

stated'hat

the deviation forms would be processed

and that the overtime worked by the

individuals was acceptable.

It was determined that the TS 7-day and 2-day overtime restrictions apply to

consecutive

days, and a review of bi-weekly pay records would not necessarily

verify these requirements

are being met.

Overtime Deviation Reports are distributed

to work group supervisors showing their employee's work hours for rolling 7-day

and 2-day periods.

Based on discussions with several supervisors, it was not

apparent to the inspector that these reports were routinely used.

Based on discussions with the inspector the licensee initiated a Condition Report

and initiated a preliminary review. The licensee determined similar weaknesses

in

the Health Physics work areas and has initiated corrective actions to resolve these

weaknesses.

C.

Conclusion

Working hours of SSES staff who perform safety-related functions were sampled in

the Operations

and Maintenance

areas.

No examples of excessive

use of overtime

were identified.

Three examples were found in the Maintenance organization where

administrative forms were not processed

in a timely manner however, this delay

was inconsequential.

07

Quality Assurance

in Operations

07.1

Effectiveness of Licensee Controls - Problem Resolution

Ins ection Sco

e 71707

The inspector reviewed a sample of approximately 300 licensee corrective action

documents,

Condition Reports (CR), Operability Determinations,

and Independent

Safety Evaluation Services

(ISES) documents.

In addition, the inspector attended

several Plant Operations Review Committee (PORC) meetings and reviewed

a

sample of approximately 40 PORC meeting activity summaries.

The inspector

attended routinely'held CR telephone conferences

in which CRs were discussed,

responsibilities assigned

and the impact on operations

assessed.

Finally, the control

room activities of the ISES were observed

and discussions

held with the ISES

control room auditor.

Observations

and Findin s

The inspector determined that the licensee was generating

a relatively large number

of CRs.

The increase

appeared

to be the result of a decrease

in the threshold for

reporting, personnel

related environmental conditions, and an increase in

management

emphasis

on the routine use of the system by plant personnel.

It was

further determined that the licensee was dedicating adequate

resources to the

process including increased visibility and attention through upper level PPSL

management.

The inspector observed the routine active participation in this proces's

by the Vice President Nuclear Operations.

The participation of upper level PPRL

management

in the CR processes,

visibly displayed

a company emphasis

on speedy

evaluation and problem resolution of safety significant issues.

Because of the

marked increase

in the number of CR documents

and issues,

a potential weakness

lies in the ability of PPSL to identify and separate

the safety significant issues from

the areas of lesser safety significance.

In general, current company efforts in this

potential area of weakness

are very good.

In a few instances,

the inspector identified weaknesses

in either the initiation of

CRs or the evaluation of specific CR deficiencies.

These instances

are assessed

by

the inspector on a continual basis for emerging trends.

One example of this type of

finding is contained in Section 04.1 of this report.

Some of the activities of the ISES control room audits mirror the NRC inspection

module 71707, directly. Other activities were individually developed

by ISES.

On a

whole, the ISES activities appear to support control room activities and the problem

resolution process adequately.

C.

Conclusions

From a programmatic standpoint, the licensee has established

and implemented

an

effective program of controls for the resolution of identified problems.

These

controls include the activities of the Independent

Safety Evaluation Services,

the

Plant Operations

Review Committee, and the visible support of corporate officer

level management.

Based on the selected sample, most CRs were resolved

effectively and were associated

with adequate

evaluations of safety significance

and operability impact.

08

Miscellaneous Operations Issues (92700)

08.1

Closed

LER 50-387 96-007:

A Division 1, primary containment isolation occurred

as the result of a loss of power to the Division

1 Reactor Protection System (RPS).

The loss of power to the RPS was caused

by a bus lockout which actuated during a

maintenance

activity. The maintenance

activity involved the connection

(landing) of

an over current relay on the alternate feeder breaker to a 4 Kv engineered

safeguard

system bus.

This event was discussed

in NRC Inspection Report (IR) 50-387,

388/96-09, and it was determined by the inspector, that the event resulted from an

incorrectly landed lead.

More specifically, it was determined that a human

performance error occurred during the connection of an electrical relay.

IR 387,

388/96-09 contained

an error and incorrectly stated that the power at which the

lockout occurred (30% vice 0% power).

This error did not affect the review

performed by or the conclusions of the inspector.

The licensee's

corrective actions

were determined to be adequate.

This failure constitutes

a violation of minor safety

consequence,

and is being treated as a non-cited violation consistent with Section

IV of the NRC Enforcement Policy.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities (62707):

MT-052-002, High Pressure

Coolant Injection (HPCI) Pump 6-

Year Overhaul, Unit 1

WAP52435

HPCI Repair

CP 031-511

Digital Computer Annual Preventive Maintenance,

Unit 1

WAC60854

4 Kv 1A204 Division 2 Relay Replacement,

Unit 1

WAC60501

4 Kv 1A204 Division 2 Rewire Degraded

Grid Test

Switches, Unit 1

~

TP 059-003

Suppression

Pool Cleaning and Inspection, Unit 1

TP-059-003

Unit 1 Suppression

Pool and emergency core cooling system

(ECCS) Suction Strainer Inspection, September

19, 1996

WA P52435

Six-Year HPCI Turbine Overhaul, September

26, 1996

WA S67577

Post Maintenance Testing For Zone III BDD17521,

September

24, 1996

WA S63817

Hydraulic Control. Unit (HCU) 26-31 Charging Water Isolation

Valve 147113-2631

Repair, October 3, 1996

~

WA C60479

Reactor Building Closed Cooling Water (RBCCW) Loop

'B'eactor

Recirculation Pump Containment Isolation Solenoid

Valve Replacement,

October 4, 1996

The inspectors observed

all or portions of the following surveillance activities

(61726):

SE 151-202

Core Spray Pump B, 1000psig Hydrostatic Test, Unit 1

SO 070-018

Standby Gas Treatment System, Unit 2

SO 149-005

Residual Heat Removal System Quarterly Valve

Exercising,

Unit 2

SE 151-003 'A'ore Spray Logic Test and Functional Check, Unit

1

SO 024-001

Monthly Operating Test 'C'mergency

Diesel Generator

SO 150-050

Reactor Core Isolation Cooling Logic Test

SE-151-001

Unit 1 Loop A Core Spray System Logic Functional

Surveillance, September

9, 1996

SE-124-107

Unit 1 Division I LOCA/LOOP 18-Month Surveillance Test,

October 8, 1996

b.

Observations

and Findin s

One of the observations

conducted

by the inspector, involved portions of the

prerequisites

and the execution of the 18-month Unit 1, Division 1, Loss of Coolant

Accident/Loss of Offsite Power (LOCA/LOOP). This comprehensive

test required

numerous teams of in plant personnel

and extensive coordination.

The inspector

noted an excellent pre-job briefing, effective coordination by the NSE test directors,

and good communication with control room operators.

c.

Conclusions

In general, the majority of the observed

maintenance

and surveillance activities

were well performed.

An exceptionally well performed activity involved the 18-

month Unit 1, Division 1, Loss of Coolant Accident/Loss of Offsite Power

surveillance test.

This comprehensive

test included an excellent pre-job briefing,

effective coordination by the NSE test directors, and good communication with

control room operators.

10

M1.2 Control Rod Drive CRD Mechanism

Re lacement

a.

Ins ection Sco

e 62707

On September 25, 1996 the inspector observed

CRD mechanism

replacement

activities and identified several weaknesses.

b.

Observations

and Findin s

On September

25, 1996 at approximately 4:00 p.m., the inspector communicated

to SSES management

several identified weaknesses

observed

during the process of

CRD mechanism replacement.

The crew demonstrating

the weaknesses

was

composed of a foreman directing the activities by headset

and two workers located

under the reactor vessel.

In addition, there was an operations engineer that was

performing an advisory function.

The following activities were observed:

~

The foreman was not correctly using the appropriate'rocedure,

MT-055-

015, to direct the activities of the workers under the vessel.

In two instances the foreman directed the workers to perform activities that

were not addressed

by the procedure.

These two activities included removal

of roller pins, and manually wrestling the CRD back and forth to unlodge the

CRD mechanism.

When questioned

by the inspector, the foreman stated that he was not

required to use the procedure or have it in front of him because

he had it

memorized.

~

When the CRD activities impacted an intermediate range monitor cable, the

occurrence was not initially documented

in the work log by the supervising

foreman and therefore, the need for an operability review was not

documented

(note: the operations engineer independently

phoned the control

room and notified them that the cable had been impacted, while the

inspector discussed

the issue with PPSL first line management).

After the

'nspector

had a discussion with SSES first line management

a work log entry

was made.

~

A bent retaining bracket was noted by the inspector and the CRD work crew

independently.

The bent bracket appeared

to be the result of the observed

work activities under the vessel that were intended to free the lodged CRD

mechanism

(see the first bullet above).

After the inspector discussed

the above issues with the first line supervisor, the

supervisor chose to stop work.

In addition, when he was notified, the control room

Shift Supervisor reiterated the stop work direction.

Work activities were

recommenced

after the crew had been instructed in proper procedure

usage

and the

bracket was replaced with a bracket from the SSES training center.

11

On September

26, at approximately 11:00 a.m., a second stop work was ordered

by the Shift Supervisor when it was discovered that six of eight bolts were removed

from an incorrect CRD (CRD 34-51 vice the correct 38-55).

One of the workers

under the vessel identified the condition, notified the foreman on his headset

and

reinstalled the incorrectly removed six bolts.

The licensee documented

the

condition on CR 96-1663, paneled

an event review team (ERT), implemented

a

number of immediate corrective actions including second check verifications, and

submitted the results of its review and corrective action recommendations

to the

Plant Operations Review Committee (PORC) for approval prior to the release of the

stop work order.

The inspector determined that the licensee's

response

and corrective actions

following the September

26 event, were strong, technically sound, and outstanding.

The PORC activities and actions were also determined to be outstanding

and

introspective.

However, the initial response

by site Maintenance

Management to

the weaknesses

identified by the inspector on September 25, was inadequate

in

that it did not fully respond to the concerns

expressed

by the inspector and did not

prevent the September

26 event.

TS 6.8.1 states that the licensee shall establish and implement procedures

recommended

in Regulatory Guide 1.33.

SSES Nuclear Department Administrative

Procedure

(NDAP)-QA-0500, establishes

approved practices for maintenance

procedures

and work plans.

NDAP-QA-0500 refers to Maintenance

Procedure

MT-

AD-501, which establishes

the procedural adherence

requirements for different

types of maintenance

procedures.

Section 6.2 of MT-AD-501, Maintenance

Procedure

Program, states that a step-by-

step conditional procedure provides specific detailed direction.

It further states that

strict adherence to the procedure exactly as written and in its entirety is required.

Finally, it states that the procedure must be in the field and on the job.

Maintenance

Procedure MT-055-001, CRD Removal, is a step-by-step

conditional

procedure that controls the removal and replacement of the CRD mechanisms

including the identification of the correct mechanism

and controls to second party

verify the correct mechanism.

Contrary to the requirements discussed

above, MT-055-001 was not used in a step-

by-step fashion in the field by the foreman directing the CRD removal activities.

Therefore, the controls to identify and verify the correct mechanism were not

effective.

This failure resulted in the wrong CRD being partially disassembled

with

the potential to negatively affect the cooling of the fuel assemblies

in the core and

spent fuel pool, and/or affect local reactivity conditions.

This is a violation, (VIO

387/96-1 0-02).

The inspector determined that the following root causes

contributed to the event:

Training - The workers were directed to memorize applicable portions of MT-

055-001 during their training at the SSES training center.

This training

12

activity left the workers with the impression that they did not have to use

the procedure

because they had it memorized.

Training - One of the foreman observed

by the inspector had been given

credit for previous work at other utilities and therefore, had not been required

to complete

a full course of training at the SSES training facility.

Work Experience - Crews that had been previously hired and trained by SSES

to perform CRD maintenance

were impacted by a recent personnel

realignment.

This resulted in the loss of approximately 17 out of 24

personnel from the CRD/HCU maintenance

crews.

The reassigned

personnel

were replaced with less experienced

contracted workers.

QA Oversight - During the periods observed

by the inspector, no QA

oversight of the work activities was observed.

Line Management

Oversight - During the periods observed

by the inspector,

there was a lack of direct line management

oversight of the foreman

directing under vessel activities.

Direct line management

oversight was

relegated to an Operations

Engineer, who was assigned to the crew without

a clear written statement of responsibilities or authority.

The incorrect CRD mechanism

did not have the control blade withdrawn and backseated

to

provide a leak seal.

If the final two bolts were removed or sheared off, allowing the CRD

mechanism flange to separate

from the bottom of the vessel,

a leak would have occurred.

The consequences

of the flange failure would

be an uncontrolled leak and an uncontrolled

reactivity addition.

The uncontrolled leak was projected by the licensee to be

approximately 300 gpm.

The potential to affect local reactivity conditions in the core

would result from the dropping blade movement.

The leak would not have been isolable

until the rod was either disassembled

from the blade or the flange was reseated

by the

hydraulic unit. If the flange was not reseated,

and if the control rod could be disassembled

from the blade, then there was a special tool (slide flange) available at the work scene that

could have been used to stop the leak.

The following factors mitigated the significance of this specific event:

Secondary containment (ventilation zones

1 and 3) was set by procedure.

In the

event of a leak, this alignment would significantly reduce

a potential release to the

public.

One Core Spray pump was operable,

as required by licensee controls for operations

with the potential to drain the reactor vessel/cavity (OPDRVC). This pump was

capable of supplying enough cooling medium to the reactor vessel to keep the core

covered and cooled during a 300 gpm leak.

The incorrect CRD mechanism

did not have the control rod uncoupled or the

position indicating probe (PIP) removed.

The licensee contended that the installed

PIP would have affected the alignment of the hydraulic removal tool enough to alert

0

13

the workers not to remove the final two bolts.

This argument does nothing to

mitigate the potential of the final two bolts shearing.

c.

Conclusion

The licensee failed to adequately

control CRD mechanism

repair activities in

accordance

with established

SSES procedures.

As a result bolts were removed

from an incorrect CRD mechanism flange.

The resulting plant condition was

identified by an SSES worker and no leak actually occurred.

There was sufficient

pump capacity and onsite emergency power available to supply water and cooling

to the core and spent fuel pool if the leak had occurred.

Secondary containment

was operable

and would have allowed a filtered vent path through SBGTS to the

environment.

M1.3

Reactor Feedwater

Pum

Re air

a.

Ins ection Sco

e 62707

On September 20, 1996, and October 1, 1996, the inspector observed

repair

activities on the 'C'nd 'A'eactor Feedwater Pumps (RFPs), respectively.

The

following procedures

were reviewed:

Weld Traveler P52338

MT-048-001, RFP Disassembly Inspection and Reassembly

WAP52338, Pump Stage Repair

S63183,

RFP Rotor Removal

b.

Observations

and Findin s

The activities were observed to be well controlled, were performed in accordance

with the applicable work plans, and were affected by knowledgeable

maintenance

and welding technicians.

The welding technicians performing the weld buildup and

milling operations demonstrated

considerable

technical skills under less than

optimum field conditions.

. c.

Conclusion

The activities involved in the weld repair and milling of the Unit

1 reactor feed

pumps were well controlled by first line management,

and were performed in an

excellent manner.

M1.4

Core Shroud Examination and Re air

a.

Ins ection Sco

e 62707

On September

11, 1996, the licensee completed

a visual and ultrasonic examination

of the core shroud assembly welds.

The inspector observed portions of the

examination and evaluation processes,

and reviewed the following documentation:

14

UT-SUS-503V5, Procedure for automated

Ultrasonic Examination of the

Shroud Assembly Welds.

EC-062-1036, SSES Unit

1 Shroud Defect Calculations, dated October

8, 1996.

Structural Integrity Associates

Inc. Report, dated October 7, 1996.

On October 14, 1996, the inspector attended

a PORC meeting that reviewed the

results of the Inservice Inspection program including the core shroud examination

results.

In addition, the following corrective action documents

were reviewed to

assess

the quality of the licensee's

corrective actions and operability

determinations:

CR-96-1486

CR-96-1565

CR-96-1567

CR-961588

CR-96-1637

CR-96-1639

CR-96-1650

b.

Observations

and Findin s

next opera

c.

Conclusion

The inspector determined that the methods used by the licensee were conservative

and the conclusions arrived at by the licensee were supported

by industry standard

analysis.

The inspector was not able to verify that Unit 1 operation beyond the

ting cycle was supported

by the current test data.

The activities involved in the core shroud evaluation and inspection were well

controlled by first line management,

met current industry standards

and were

performed in an excellent manner.

M1.5

~Scaffoldin

aa

Ins ection Sco

e 62?07

The inspector observed/evaluated

the construction of several scaffolds near and/or

surrounding safety related equipment.

The licensee process for managing scaffolds

is contained

in Maintenance

Procedure

MTAD-504, Scaffolds.

b.

Observations

and Findin s

It was determined that several of the scaffolds were in place for long periods of

time (months).

In addition, the need for the particular scaffolds had not diminished

and was expected to continue.

Because of the permanent

nature of certain

scaffolds, the inspector determined that they were acting as defacto plant

modifications.

It was further determined that MTAD-504 ensured that erected

scaffolding was seismically qualified, but did not fully meet 10 CFR 50.59, in that

the MTAD did not fully ensure that the erected scaffolding would not negatively

0

15

impact nearby safety related equipment during each previously analyzed

FSAR

Chapter 15 design basis accident.

These issues were discussed with the licensee who agreed with the finding and

implemented

a number of corrective actions.

These actions included:

1)

The establishment

of a task force to address the issue.

2)

A walkdown of existing scaffolds by civil engineers.

3)

Submission of project plans to an SSES Project Review Team

screening

on or before October 17, 1996.

4)

The establishment

of additional controls on long term scaffolding

requests.

There were no conditions identified by the inspector, that clearly impacted the

present operation of safety related equipment.

Subsequent

to the inspector

identifying the issue to the licensee, the licensee performed

a walkdown of erected

scaffolds, removed some unneeded

scaffolds and determined that there were no

present instances of impact on the operation of safety related equipment.

c.

Conclusions

PPSL mana gement response

was comprehensive

and identified no present impacts

on the safe operation of plant equipment from existing scaffolds.

Therefore, this

failure to consider the effects of plant modifications in accordance

with 10 CFR

50.59, constitutes

a violation of minor consequence

and is being treated as a Non-

Cited Violation consistent with Section IV of the NRC Enforcement Policy.

M1.6

Overall Conclusions

on Conduct of Maintenance

Maintenance activities were generally well controlled.

The Unit 1 LOCA/LOOP

testing observed was well coordinated

and executed.

One violation and several

weaknesses

were identified during control rod drive mechanism maintenance

activities.

Programmatic weaknesses

were identified in non-cited violations for the

control of scaffolds and the control of temporary storage of materials.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Safet

Relief Valve Set Screw Lockwire

a.

Ins ection Sco

e 62707

During the Unit 1 refueling outage the inspector performed walkdown inspections,

inside containment, of ongoing maintenance

activities and general equipment

condition.

16

b.

Observations

and Findin s

The inspector found that the set screw lockwire and the lead seal for the 'S'afety

relief valve (SRV) were broken.

Following the repair, testing, and adjustment of an

SRV, the refurbishment company installs a lockwire and lead seal to indicate the

final adjustment

has been made.

The 'S'RV was last refurbished during the Unit

1 Spring 1995 outage.

The inspector questioned

whether the settings of either

SRV set screw had been changed

since its adjustment.

The torque of the 'S'RV set screws was verified by the licensee to be the required

250 ft-Ibs and the lockwire/seal was replaced.

The set screws are used to maintain

the SRV nozzle ring and adjusting ring positions following the calibration of the SRV

setpoint and during the installation process.

Adjustment of these rings requires

access through the valve's outlet flange and would require removal of the SRV

tailpipe.

Based on the fact that the set screws were found to be torqued by the

licensee, the inspector considered it unlikely that vibration during the last operating

cycle could have affected these adjustments.

The licensee, concluded that work

activities conducted

between and around the SRVs was the cause of the. broken

lockwire. The licensee's inspection of set screw lockwires on the remaining 15

SRVs did not identify any additional problems.

c.

Conclusion

The licensee's followup in response

to a broken lockwire and seal discovered

on set

screws for the 'S'afety relief valve was good.

M8

Miscellaneous Maintenance Issues (92903)

M8.1

Closed

Unresolved Item

URI 50-388 95-12-01

Hi h Pressure

Coolant In'ection

HPCI On-line Maintenance

On June 26, 1995, the licensee commenced

a four day on-line maintenance

work

window for the Unit 2 HPCI system.

The work scope of the outage increased the

risk consequences

for analyzed events and increased the core damage frequency.

The licensee evaluated the increase

in risk and risk consequence

and provided

adequate

compensatory

measures.

Four issues were identified in NRC IR 50-

388/95-12 that occurred during the performance of the maintenance

window. This

URI was opened to review the licensee's corrective actions for these four issues.

The inspector reviewed the licensee's completed corrective actions which included

improvements

in scheduling techniques,

personnel training, and procedural

upgrades.

The licensee's corrective actions were determined to be adequate.

In

this case, the maintenance

procedure quality and adherence

concerns constitute

a

violation of minor consequence

and are being treated as a Non-Cited Violation

consistent with Section IV of the NRC Enforcement Policy.

17

M8.2

Closed

URI 50-387 95-05-01:

Observation Of Activities On The Refuel Floor

The inspector observed the movement of new fuel from the fuel vault to the spent

fuel pool in preparation for the Unit 1 8th refueling outage.

The inspector found

that a procedure step for second verification of the bundle serial number was not

being performed.

After identification, an individual was assigned to verify the bundle serial numbers

as required by the licensee's

procedure.

A video tape of the fuel pool was used to

verify all bundles were moved to their proper location.

In addition to the CR process

review, an investigation of this issue was performed by the ISES group.

The

licensee's corrective actions included ISES recommendations

and established

periodic training, better definition of the supervisory assignments

and enhancement

of procedural controls.

The inspectors did not identify additional problems of this

type during the remainder of the Unit 1 8th Refueling Outage.

New and irradiated

fuel movements were observed during this inspection period (Unit 1 9th Refueling

Outage) and the recording of bundle serial numbers was observed.

Based on the

licensee's corrective actions, the failure to implement required procedure steps

constitutes

a violation of minor consequence

and is being treated as a Non-Cited

Violation consistent with Section IV of the NRC Enforcement Policy.

I

III. En ineerin

Conduct of Engineering

U date - URI 387 388 96-06-01

Containment Secondar

B

ass Leaka

e

~73051

The adequacy containment secondary

bypass leakage was identified as an issue in

several licensee corrective action documents

(CR). The need for resolution of

potential design discrepancies

was detailed in NRC Inspection 50-387, 388/96-06.

The licensee's

plan for resolving CR-96-46, 310, 356, 1359, 504, 522, 1038,

1360, and 1407 was included in an action plan dated October 10, 1996.

The

inspector reviewed the conclusions

and evaluations proposed

by site engineering to

the PORC on October 14, 1996.

In addition, a copy of the action plan was

provided to NRC Licensing (NRR) for review under TAC numbers 96641 and 96642.

The inspector determined that the plan appeared

to be complete and was

thoroughly reviewed by PORC.

The plan included proposed

TS changes to account

for a potential unreviewed safety question.

The inspector was not able to

determine if the increase from 5 to 9 SCFH of leakage was appropriate without a

prior review of the methodology by NRR, which will be conducted

under the TAC

numbers listed above.

This issue is being tracked by unresolved

item 387, 388/96-

06-01.

IV. Plant Su

ort

Radiological Protection and Chemistry (RP8cC) Controls

The inspector performed

a review of the radiological controls program, with special

emphasis

on the controls implemented for the Unit 1 refueling outage.

Specific

areas reviewed included:

maintaining radiation exposures

as low as is reasonably

achievable

(ALARA);control of radioactive material and contamination; external

exposure controls; facilities and equipment; staff training; organization and

administration; and program audits and appraisals.

In addition, the inspector

reviewed the radiological controls implemented for historical work including Unit 2

reactor water clean-up (RWCU) pump work performed in January 1996 and

transverse

incore probe (TIP) drive box work performed in December 1995.

The

inspector also reviewed licensee response

to a previous NRC violation and an NRC

unresolved item, and an evaluation of facility condition versus the UFSAR was

performed.

ALARA

lns ection Sco

e 83750

The inspector performed

a review of the program to maintain radiation exposures

ALARA,including the use of radiation exposure

goals and ALARAreviews.

The

inspector gathered information by a review of a handout used at the September

25,

1996, Station ALARACouncil meeting; ALARAreviews performed for in-service

inspections

and control rod drive (CRD) exchanges;

inspections

in the plant; and

through discussions with cognizant personnel.

Observations

and Findin s

A station goal had been set to maintain total station dose to less than 265 person-

rem for 1996.

This included 140 person-rem for the Unit 1 fall refueling outage.

The inspector noted that as of September 26, 1996, at 07:30, the total outage

dose was 90.95 person-rem.

Major contributors to this total were CRDs, drywell

snubbers,

drywell scaffolding, reactor pressure

vessel disassembly,

drywell

shielding, and drywell in-service inspection activities. At the time of the inspection,

the dose accumulation rate had increased

due to CRD exchanges.

The inspector

noted that this had been accounted for in the dose goal.

Person-rem

dose for

individuals, radiation work permits, plant areas,

and station totals were being

closely tracked as evidenced

by a review of a daily and cumulative dose graph, daily

printouts of RWP totals, a weekly evaluation of challenges

and successes,

and a

weekly review of person-rem

breakdown by work group.

The inspector also selectively reviewed ALARApre-job reviews included in RWP

packages.

ALARAreviews included person-rem estimates,

work planning

information, external and internal exposure controls, health physics operational

concerns, dosimetry and radiological monitoring, anticipated dose rates, additional

comments,

and a work flow synopsis.

ALARApackages

were detailed, included

19

specific instructions from lessons learned from previous jobs, and were overall very

good.

Through discussions with members of the ALARAstaff, the inspector observed that

extensive planning had been performed for outage activities, and ALARAmeasures

such as radiation work permit controls, temporary shielding, and system flushes

were effectively implemented.

C.

Conclusions

The inspector concluded that the ALARAprogram was effectively implemented.

This was evidenced

by excellent use of ALARAdose goals, extensive planning, use

of RWP controls, use of temporary shielding, system flushes, and postings and

verbal communications.

R1.2

Control of Radioactive Material and Contamination

ae

Ins ection Sco

e 83750

The inspector performed

a review of the control of radioactive material and

contamination.

Information was gathered

by direct observation of personnel

and

equipment contamination monitoring practices during tours through the facility.

Observations

and Findin s

During tours of the facility, the inspector examined radioactive material packages,

and noted that all packages

(e.g., bags, containers,

or boxes) of radioactive material

were appropriately labeled as radioactive material.

All contamination monitoring equipment observed to be in-use including friskers,

personnel contamination monitors (PCMs), tool contamination monitors (TCMs), and

continuous air monitors (CAMs) appeared to be in good condition, and records

showed that they were within calibration.

The inspector noted that the number of access/egress

points to the radiologically

controlled area had been reduced to two locations; the Unit 2 turbine (South)

access,

and the control enclosure access.

This change

had been implemented to

better control radioactive material and contamination.

All personnel were authorized

to use the Unit 2 turbine access

and the control enclosure access was limited to

personnel from operations,

chemistry, health physics, and security.

In addition, a

policy had recently been implemented to allow station personnel to monitor personal

items such as note paper and pens, using tool contamination monitors (TCMs).

Health physics personnel

provided direct oversight at the Unit 2 access point, and

monitored the control enclosure access

by video and video tape.

The inspector

observed

health physics personnel providing coaching and counseling to station

personnel when contamination monitoring deficiencies were observed.

In the event

that contamination monitoring deficiencies were identified by video/video tape

review, appropriate followup actions such as interviews and followup surveys were

20

performed to determine if contamination

had been improperly released.

Based on

this review, the inspector concluded that contamination control practices and health

physics monitoring of contamination control practices were very good.

C.

Conclusions

Based on this review, the inspector made the following conclusions.

~

Radioactive material control practices were good as evidenced

by appropriate

labeling of radioactive material packages

including bags, containers,

and

boxes.

~

Contamination monitoring equipment were well maintained as evidenced

by

very good equipment condition, and instrument calibration records.

~

Health physics oversight of contamination monitoring practices was excellent

and showed improvement.

This was evidenced

by the elimination of multiple

radiological control area (RCA) egress points, and very close health physics

oversight of personnel

and equipment contamination monitoring at the Unit 2

RCA access/egress

point.

R1.3

External Ex osure Controls

a.

Ins ection Sco

e 83760

The inspector performed

a review of external exposure controls including use of

radiological boundaries,

drywell shielding, and drywell pipe flushing.

Information

was gathered through tours of the facility, review of results of the effectiveness of

installed shielding and pipe flushes, and through discussions with cognizant

personnel.

b.

Observations

and Findin s

The inspector toured the Unit 1 reactor building including the Unit 1 drywell and

refuel floor. Radiological boundaries

were well defined, and based on a review of

radiological surveys, radiation areas and high radiation areas were properly posted.

The inspector noted good use of informational posting including dose rate range

posting, and Unit 1 drywell maps that identified areas with elevated dose rates and

low dose areas.

During tours of the Unit 1 drywell, the inspector observed multiple temporary

shielding installations.

Approximately 24,000 pounds of temporary lead shielding

and associated

hardware were installed in the Unit 1 drywell. Shielding packages

were well designed

and installed, appeared

neat and orderly, and provided evidence

of detailed planning.

Based on a review of radiation surveys,

a pre- and post-

shielding dose rate summary, and selective radiation dose rate verification surveys

performed by the inspector, the inspector concluded that the drywell shielding

21

program was well planned and managed,

and shielding packages

were effective in

reducing general area dose rates.

The inspector also performed

a selected review of the effectiveness of drywell

system flushes.

The inspector reviewed an outage schedule

and noted that specific

"flushes," designed to reduce radiation dose rates in the drywell, were integrated

into the outage schedule.

The inspector reviewed documentation

of pre- and post-

radiation survey results for the "flushes," and noted significant dose rate reductions

were achieved.

Dose rates at a distance of 30 centimeters were reduced on the B

recirculation pump drain line from 1000 mrem/h to 150 mrem/h; on B core spray

piping from 1000 mrem/h to 80 mrem/h, and dose rates at the N2F recirculation

discharge

nozzle were reduced from 6000 mrem/h to 600 mrem/h.

Based on this

review, the inspector concluded that drywell flushes were well planned

and

effectively implemented.

b.

Conclusion

Based on this review, the inspector made the following con'elusion.

~

External exposure controls were excellent including use of informational

postings, use of temporary shielding, and ALARAsystem flushes.

R1.4

Use of Flashin

Li hts for Access Control to Hi h Radiation Areas

a,

Ins ection Sco

e 83750

The inspector reviewed the use of flashing lights for access control to high radiation

areas.

The inspector gathered information by reviewing Technical Specification 6.12, "High Radiation Area;" Nuclear Department Administrative Procedure

NDAP-

00-0626, "Radiologically Controlled Access and Radiation Work Permit (RWP)

System," Rev. 4; procedure

HP-TP-311, "Locking, Barricading, 5 Key Control," Rev.

11; procedure

HP-TP-310, "Posting and Labeling," Rev. 16; NRC Information Notice 88-79, "Misuse of Flashing Lights For High Radiation Area Controls," 10/7/88;

radiological survey data for the Unit

1 drywell and 704'levation equipment space.

The inspector also performed tours through the Unit 1 drywell, and discussed

high

radiation area access controls with cognizant personnel.

b.

Observations

and Findin s

Technical Specification 6.12, "High Radiation Area," and procedural guidance,

requires areas with dose rates greater than or equal to 1000 mrem per hour to be

controlled with barricades

and locked doors.

In the event the area is located within

a large area where no enclosure could reasonably

be constructed,

then access

control is achieved by roping the area off, conspicuously

posting the area, and

activating a flashing light as a warning device.

i

22

The inspector noted that, in general, access control to high radiation areas with

dose rates greater than 1000 mrem per hour were controlled with barricades

and

locked doors.

However, access to several locations within the Unit 1 drywell and

one location in the Unit 1 reactor building, 704'levation equipment space, with

dose rates in excess of 1000 mrem per hour were controlled by roping the area off,

posting the area as a high radiation area, and activating a flashing light.

For

example, due to hydrolasing/flushing

activities performed on the Unit

1 scram

volume discharge

header,

a high radiation area with dose rates of 1400 mrem per

hour was created in piping located in the Unit 1 704'levation equipment space.

The radiological controls staff initiated plans to flush the piping to remove the

elevated dose rates, and during the interim, controlled access with a rope boundary;

a high radiation area posting; a flashing warning light; a radiation work permit; use

of alarming dosimetry; radiological briefings; and health physics monitoring of

personnel

accessing

the larger equipment space that surrounded

the area.

The inspector was informed that other effective measures

for controlling access to

this area had been considered

(e.g., locking the outer 683'quipment

space doors,

or installing locking ladder blocks).

However, the use of flashing warning lights

combined with additional access controls was thought to be reasonable

while

providing positive access control.

Licensee staff also informed the inspector that a radiological controls information

document

(Rad Safety Note) had been prepared for distribution to all station

personnel

~ This was intended to serve as an additional training method to inform

personnel of the use of flashing warning lights to control access to high radiation

areas.

The inspector noted this as a good initiative.

The inspector concluded that the licensee's

use of flashing warning lights combined

with radiation work permit controls for access to high radiation areas was

reasonable

and represented

positive exposure control.

No examples of improper

entries into high radiation areas controlled with flashing warning lights were

identified.,

C.

Conclusions

Based on this review, the inspector made the following conclusion.

~

The use of flashing warning lights combined with radiation work permit

requirements to control access to high radiation areas, was reasonable,

represented

positive exposure control, and was in compliance with Technical Specification 6.12, "High Radiation Area."

R1.5

Res

onse to Alarmin

Dosimetr

a.

Ins ection Sco

e 83750

The inspector performed

a review of licensee response to alarming personnel

dosimetry.

Information was gathered

by a review of HP-TP-126, "Use of the Real

23

Time Dose Tracking System," Rev. 3; interviews with health physics technicians;

and a review of actions taken in response

to personnel dosimetry that alarmed

during Unit 1 control rod drive exchanges

performed the morning of September 25,

1996.

Observations

and Findin s

During a review of the radiological controls implemented for Unit 1 control rod drive

(CRD) exchanges,

the inspector was informed that on the morning of September

25, 1996, several individuals received alarms on their personal dosimetry while

working on CRD exchanges.

The inspector performed a review to determine if

appropriate actions were taken in response to alarming dosimetry.

Health physics procedure

HP-TP-126, "Use of the Real Time Dose Tracking

System," Rev. 3, requires workers to evacuate their immediate work area and notify

Health Physics whenever their dosimetry alarms.

The procedure

also requires health

physics to determine the cause of the alarm.

'I

On the early morning of September

25, 1996, two maintenance

workers were

located on the Unit 1 drywell subpile room carousel,

and were involved in CRD

exchanges.

A senior health physics technician was providing constant health

physics coverage,

and undervessel

activities were being monitored remotely with

audio and video communications

by several maintenance

personnel,

and a

representative

from the operations department.

Undervessel

maintenance

personnel

were working under radiation work permit (RWP) 1996-1356,

"CRD Exchange:

Undervessel Work," personal alarming dosimetry (PAD) had been relocated to the

head (location of whole body exposed to the highest dose rate), and the PAD dose

limit was automatically set at 400 mrem during RWP sign-in.

According to the health physics technician that provided constant coverage for the

job, on the morning of September 25, 1996, two maintenance

workers had been in

a 200 mrem/h area for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> when one of the individuals PAD

alarmed.

The alarm was immediately detected

by the health physics technician in

the field, and by the maintenance

and operations

CRD support team that were

remotely monitoring activities by video.

The CRD support team was not sure if the

individual heard the PAD alarm, so they informed the individual that he had received

an alarm on his dosimetry, and instructed the individual's to contact health physics.

The health physics technician responded

to the alarming dosimetry by performing a

radiation survey to identify any unusual dose rates in the work area; no unusual

dose rates were found.

The HP technician then checked the individual's dosimetry

and determined that the dosimeter alarmed because

the 400 mR alarm set point had

been exceeded.

The technician then concluded that no unusual conditions existed

and that the 400 mR PAD alarm setpoint had been exceeded

because

the individual

had worked in a 200 mR/h area for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

The HP technician then

communicated

his findings by radio to HP supervision.

The HP technician and HP

supervision then determined that since they knew the reason for the alarm, the

individual was not in danger of exceeding

an administrative or regulatory dose limit,

and constant health physics coverage was being provided, then the individual

0

should continue working to place his work in a safe condition.

The HP technician

then informed the maintenance

technician to continue working to place the CRD

exchange

machine in a safe condition, and then to leave the work area.

While

exiting the area, the second maintenance

technician received an alarm on his PAD.

The highest PAD exposure recorded was 440 mR.

The health physics technician informed the inspector that the PAD alarm dose

setpoint was used as a tool to identify when workers exceeded

an established

dose,

and not as a dose limit.

The inspector noted that the actions taken in response

to the PAD alarm were in

compliance with procedural guidance

and were appropriate.

The individual with a

dosimeter in an alarm status notified the HP technician; the HP technician

determined the cause of the alarm and informed HP supervision;

HP supervision

determined that the individual was not in danger of exceeding

an administrative or

regulatory dose limit, and authorized the HP technician to allow the workers to

remain in the area in order to place their work in a safe condition; and the

maintenance

workers placed their equipment in a safe condition, and left the area.

C.

Conclusions

Based on this review, the inspector made the following conclusions.

Procedural guidance for personnel

responding to alarming dosimetry was

adequate.

Personnel

actions taken in response to alarming dosimetry were very good.

This included notification of health physics; performance of radiological

surveys to determine the cause of PAD alarms; evaluation of individuals dose

status after initiation of a PAD alarm; and health physics instructions to

personnel

concerning the need to evacuate work areas after a PAD alarm

occurred.

R2

Status of RP8cC Facilities and Equipment

a.

Ins ection Sco

e

The inspector toured the Unit 1 and 2 reactor buildings, the Unit 1 drywell, and the

Unit 1 turbine building to evaluate radiological control boundaries

and housekeeping.

b.

Observations

and Findin s

In general, housekeeping

was good and radiological boundaries

were clearly

delineated

and well maintained.

Housekeeping

and radiological boundary

deficiencies were identified on 729'levation of Unit 1 turbine deck, and at the

683'ntrance

to the Unit

1 suppression

pool.

Examples included unsecured

cables

and cords draped across contaminated

area boundaries,

materials stored in clean

areas with edges partly in a contaminated

area, and miscellaneous

supplies,

25

materials, and trash lying in aisles and walkways.

Upon notification, radiological

boundary deficiencies were corrected,

and improvements were made in

housekeeping.

Finally, no obvious signs of degraded

material conditions in rooms or

equipment were identified.

C.

Conclusions

Based on this review, the inspector made the following conclusion.

~

Overall conditions of housekeeping,

and radiological boundaries

in the Unit

1

and 2 Reactor buildings, the Unit 1 Drywell, and the Unit 1 Turbine building

were good.

R5

Staff Training and Performance in RP8cC

a.

Ins ection Sco

e 83750

The inspector performed

a review to determine if lessons

learned and industry

events were being incorporated into health physics (radworker) training, and if

contract health physics technicians brought in to support the Unit

1 outage were

appropriately trained and qualified.

Information was gathered

by a review of lesson

plans, resumes

and training records, and through discussions

with cognizant

personnel.

b.

Observations

and Findin s

The inspector reviewed lesson plan HP-002, "Health Physics Level II," Rev. 5, and

noted that multiple examples of lessons

learned and industry events were included

in training provided to workers who were permitted unrestricted access to the

ra8iologically controlled area (RCA).

The inspector was informed that 87 contract health physics technicians,

each with

at least two years experience

had been brought in to support the Unit 1 refueling

outage.

Nine names were randomly selected from a list of contract health physics

technicians,

and the inspector requested

documentation

of qualification and training.

Based on a review of resumes,

each of selected individuals had greater than two

years experience

as a health physics technician.

Records showed that all selected

individuals had passed

the Susquehanna

Health Physics entrance exam or passed

the Northeast Utilities Health Physics exam within two years.

Finally, records of

procedure

and task qualification sign-offs were available and complete.

C.

Conclusions

Based on this review, the inspector made the.following conclusions:

26

~

Radworker training was excellent in that lessons

learned and industry events

were included in training provided to workers permitted unrestricted access

to the RCA.

~

Health physics technicians brought in to support the Unit 1 refueling outage

were qualified and appropriately trained, and training records were excellent.

R6

RPSC Organization and Administration

a.

Ins ection Sco

e 83750

The inspector reviewed the organization and administration of the health physics

organization during the refueling outage.

Information was gathered by a review of a

health physics and ALARAorganization chart, attendance

at the night shift turnover

meeting, observations

in the plant, and through interviews with cognizant

personnel.

b.

Observations

and Findin s

Health physics oversight of work and contractor health physics technician

performance,

were primarily accomplished

by upgrading experienced

Level II Health

Physics Technicians to the position of Assistant Foreman-Health

Physics, and

assigning these individuals to key outage work areas or projects.

For example, day

and night shift area coordinator positions were established for the following: Shift

Supervisor, Drywell, Refuel Floor, Reactor Building, Balance of Plant, Radwaste,

and

Maintenance

Pool. Day shift area coordinator positions were also established for the

Turbine Building and Training.

The inspector attended two shift turnover meetings,

interviewed six area coordinators,

and observed

health physics communications

in

the plant.

Assistant Foremen were extremely knowledgeable of planned work,

available resources,

and radiological conditions and controls for the areas they were

assigned to.

In addition, Assistant Foremen maintained close oversight of contract

health physics technicians

and provided appropriate directions when needed.

The

inspector concluded that the process for upgrading experienced

Level II health

physics technicians to the position of Assistant Foreman-Health

Physics, in order to

allow for better coordination and control of outage work, and better oversight of

contract health physics technician performance was effective, and noted as a

program strength.

Similarly, the ALARAstaff was increased to a total of five positions during the

outage with support from the corporate technical staff, technical training, and

health physics.

ALARAstaff members were assigned

responsibility for ALARA

planning and coordination on the refuel floor, for in-service inspection and valve

work, drywell work and shielding, and for balance of plant work.

Based on

interviews, the inspector concluded that these individuals were knowledgeable

of

planned work, and were effectively coordinating and implementing ALARAcontrols.

27

C.

Conclusions

Based on this review, the inspector made the following conclusion.

~

The process of upgrading Health Physics Level II technicians to Assistant

Foremen for outage work allowed for very good oversight of work and

contract health physics technician performance.

~

ALARAstaff members were knowledgeable

of planned work, and were

effectively coordinating and implementing ALARAcontrols.

R7

Quality Assurance in RP&C Activities

Ins ection Sco

e 83750

The inspector reviewed quality assurance

and self assessment

oversight of the

radiological controls organization.

Information was gathered by a review of Audit

96-007, "Health Physics Program," April 8, 1996, an "Assessment

of 1996 Trends

in Condition Reports," dated September

3, 1996, a selected review of condition

reports, and thorough interviews with cognizant personnel.

Observations

and Findin s

Audit 96-007, "Health Physics Program," dated April 8, 1996, was performed from

February 12- March 11, 1996, and included a review of radiological surveys,

RWP

processing

and controls, respiratory protection, internal and external dosimetry,

personnel training, and radiological postings.

The audit was conducted

as a "limited

scope" audit, because

other health physics program areas were being addressed

in

other audits/assessments

(e.g., NAS-Independent

Safety Evaluation Services

Evaluation No.95-041).

The audit concluded that the health physics program was

being effectively implemented.

One finding and ten observations/recommendations

for consideration were identified. The finding noted that six Site Modification Group

(SMG) Engineers

had not received Engineering ALARATraining (course number

EG011).

Resolution of this finding was being addressed

and tracked by Condition

Report No. 96-0219.

The inspector noted that audit observations/recommendations

were insightful and well developed.

Based on a review of the audit results, the

inspector concluded that audits were effectively used to identify program

deficiencies.

The inspector also reviewed an assessment

performed to evaluate trends in

condition reports (CRs) related to radiological controls entitled "Assessment of 1996

Trends in Condition Reports," dated September

3, 1996.

This report indicated that

from March 5, 1995, to December 31, 1995, 789 CRs were written.

Of these, only

12 (1.5%) concerned

radiological protection.

From January

1, 1996, to August 23,

1996, 1294 CRs were written. Of these, [178] (=14%) concerned

radiological

protection.

This indicates

a dramatic increase

in the generation of CRs related to

radiological protection.

The significance of the HP CRs written in 1995, and in

1996 from January to August 23, 1996, were evaluated

using a four-level

0

28

significance model.

The model assigned

significance to CRs using the following

categories:

Level 1-Significant, Level 2-Important, Level 3-Minor, and Level 4-Not a

Deficiency. The licensee reported that the majority of the 1995 CRs would have

been assigned to the Level

1 and Level 2, significance categories.

This was

compared to 178 HP CRs initiated from January to August 23, 1996, with the

majority being in the Level 3 and Level 4 significance categories:

Level 1-3%, Level

2-11%, Level 3-68%, and Level 4-18%.

The license also correlated the time at

which the increase

in the HP CR generation rate occurred to management

efforts to

"lower the threshold" for initiating condition reports.

Based on this data, the

licensee concluded that increases

in the rate of generation of HP condition reports

were attributed to management

efforts to lower the initiation threshold for CRs; the

majority of HP CRs were of lower safety significance; and the volume of HP CRs

was not indicative of an adverse trend in the significance of deficiencies in the

radiological protection program.

Based on a review of 1996 condition reports, and discussions with Health Physics

technicians,

and Quality Assurance

and Health Physics supervision, the inspector

concluded that the overall increase

in numbers of condition'reports appeared

to be

the result of a lowering of the threshold for initiating condition reports.

However,

the number of condition reports related to deficiencies in high radiation area

barricades

and postings had increased

since 1995

~ Based on a review of a list of

condition reports for 1996, the inspector identified approximately 22 condition

reports pertaining to deficiencies in barricading, postings, or locking doors to high

radiation areas, that were written between the period of January

1, 1996 to July

31, 1996.

Although none of these events have had a significant radiological

consequence

(e.g., overexposure

or significant unplanned

exposure), the number of

these events suggest

an increase in the significance of health physics related

condition reports from the year 1995 to the year 1996.

The inspector also selectively reviewed 25 condition reports related to radiological

controls.

The inspector noted that the threshold for initiation of CRs appeared

low,

that causal factors and root causes were being identified, corrective actions were

being evaluated

and identified, and corrective actions were being implemented.

Based on this review, the inspector concluded that the condition reporting system

was very effective.

The inspector did identify one condition report, involving an un-

barricaded

and un-posted

access to a high radiation area, that warranted additional

review (CR-1371).

The NRC review of this condition report appears

in Section R8.5

of this report.

Conclusions

Based on this review, the inspector made the following conclusions.

~

Quality assurance

audits were broad in scope,

and effectively used to

identify program deficiencies.

29

~

The increase

in numbers of condition reports related to radiological controls

appears to be related to management

efforts to lower the threshold for

writing condition reports.

~

Although none of the condition reports that documented

deficiencies in high

radiation area postings,

barricades,

or locked doors had significant

radiological consequences

(e.g., overexposure

or significant unplanned

exposure), the number of these events suggest

an increase

in the

significance of health physics related condition reports from the year 1995 to

the year 1996.

~

The condition reporting system was effectively used to identify, evaluate,

and resolve program deficiencies.

R8

IVliscellaneous RP&C Issues

R8.1

Transverse

Incore Probe

TIP Work In December 1995

a.

Ins ection Sco

e 83750

The inspector reviewed the radiological controls implemented for work performed in

December 1995, on the transverse

incore probe (TIP) drive system.

The inspector

reviewed the radiological controls implemented on this job through interviews with

cognizant personnel

and reviews of procedures.

b.

Observations

and Findin s

In late 1995, Susquehanna

Steam Electric Station had entered

a four-hour technical

specification limiting condition of operation

(LCO) due to an inability to isolate

containment.

A traversing incore probe (TIP) drive was stuck and had to be

manually retracted into it's shielded location.

Dose rates from the TIP drives have

the potential to be very high and have created problems in other plants.

The

inspector noted that the radiological work performed on the TIP system was

performed using a general radiation work permit (RWP), and not under a specific

RWP which would include specific radiological requirements.

The inspector noted

that NDAP-00-0626, Rev 5, "Radiologically Controlled Area Access and Radiation

Work Permit (RWP) System," Section 6.2.2.b (2) required a job specific RWP,

approved by the Radiological Operations Supervisor, for access to areas with dose

rates greater than 10,000 mrem/h.

However, Section 6.2.2.b, of the same

procedure,

states the following.

"NOTE:

In unusual conditions as determined by Shift Supervision,

a

Qualified/Certified Level II Health Physics Technician providing

constant coverage with a dose rate meter, may be used in lieu of a

job specific RWP."

Based on interviews, it was determined that shift supervision requested

health

physics to support TIP drive box work during a four hour LCO; a qualified Level II

30

health physics technician was assigned to provide constant coverage for the work;

the health physics technician used

a dose rate meter; and the technician signed-on

to a general RWP.

In addition, it was determined that radiological briefings were

performed, remote radiation monitoring equipment were utilized, and supervisory

personnel provided constant oversight towards the end of the job.

Based on

discussions

with cognizant personnel,

radiological control measures

were

appropriate

and no adverse consequences

occurred.

Conclusions'he

inspector concluded that although advanced

planning and use of a specific

radiation work permit for jobs with the potential for high radiation levels are

desirable, the work performed on the traversing incore probe (TIP) system in late

1995, was performed in accordance

with approved procedures,

and appropriate

radiological control measures

were implemented.

No violations of NRC

requirements were identified.

Reactor Water Clean-u

RWCU Pum

Work In Januar

1996

Ins ection Sco

e 83750

The inspector reviewed the radiological controls implemented on a job performed in

January of 1996, involving the disassembly

and inspection of the Unit 1 reactor

water cleanup (RWCU) pump and discharge check valve.

Specifically, the inspector

reviewed hot particle (discrete radioactive particle) controls, use of respiratory

protection, and air sampling.

Information was gathered by a review of radiation

work permit (RWP) number 1996-0045, revisions 0, 1, 2, 3, and 4; ALARA

reviews; radiological survey data; and interviews with cognizant personnel.

Observations

and Findin

s

The inspector reviewed the following radiation work permit revisions.

Hot Particle

Zone

~Yee No

Rev.

RWP No.

RWP Deecri tion

No

0

1996-0045

Disassemble

RWCU pump motor and discharge

check valve.

No Pump Breach on this Revision

Yes

No

1

1996-0045

Disassemble

and inspect RWCU motor and pump

2

1996-0045

Disassemble

and inspect RWCU motor and pump

Yes

3

1996-0045

Disassemble

and inspect RWCU motor and pump

Yes

4

1996-0045

Disassemble

and inspect RWCU motor and pump

31

The inspector noted that hot particle control zones were used on RWP 19S6-0045,

revisions 1, 3, and 4; but not on revisions 0 and 2. Health physics procedure

HP-

TP-511, "Hot Particle Controls," Rev. 2, provided guidance for monitoring and

controlling hot particles (discrete radioactive particles).

The procedure was

designed to implement controls to minimize the transfer of hot particles to

personnel,

equipment and work areas,

and to account for exposures

received from

hot particles,

HP-TP-511, Rev. 2, Section 9.1.1 stated that "hot particle control

zones shall be set up to minimize the spread of hot particles...and

should include

primary/secondary

contaminated

system breaches

when there is a potential for Hot

Particle exposure

as directed by HP supervision."

The inspector noted that although

jobs such as RWCU pump breaches

have the potential for hot particle exposure,

HP-

TP-511 did not specifically require a hot particle zone to be established for RWCU

pump breaches;

it required HP supervision to direct when a hot particle control zone

was necessary.

During interviews, the inspector was informed that Rev. 0 of RWP 1996-0045, did

not require hot particle zone controls because it did not involve a pump breach; Rev.

1 required hot particle zone controls because

it involved a pump breach; Rev. 2 did

not require hot particle zone controls because

no hot particles were found during

the initial pump breach; and Revs. 3 and 4 required hot particle zone controls

because

high contamination

and fine, dust-like metal shavings were encountered.

Based on a review of radiological survey data, the inspector noted that although

high contamination was present (e.g., 2,400 mrad per hour per 100 cm'n the

pump flange on January 22, 1996), no discrete hot particles were identified during

the course of the work.

The inspector noted that it is generally prudent to use additional contamination

controls, similar to hot particle controls (e.g., use of contamination buffer zones and

additional contamination monitoring of personnel

and areas), for jobs involving high

contamination, with the presence

of very fine, dust-like metal shavings.

Although

the elimination of hot particle controls on RWP 1996-0045, Rev. 2, showed

a lack

of prudence,

no procedural violations or consequential

radiation exposures

were

identified.

The inspector also reviewed use of respiratory protection for RWCU pump work.

RWP 1SS6-0045,

"Disassemble

and inspect RWCU motor and pump," Rev. 1,

required use of decontamination,

wetting areas to suppress

dust generation,

and

use of a high efficiency particulate air (HEPA) filtration unit to minimize airborne

radioactivity, and eliminate the need for respiratory protection.

During removal of

the pump diffuser and impeller, an air sample was obtained which indicated an

airborne radioactivity concentration

up to 0.66 times the derived air concentration

(DAC) of radionuclides for occupational

exposure.

Based on these results, on

January

19, 1996, an "ALARAIn-progress Review" was performed, which

documented

the need for respiratory protection.

A filter respirator with a protection

factor of 50 was selected for RWP 1996-0045, Rev. 2, rather than a powered air

purifying respirator (PAPR) with a protection factor of 1000, because

a protection

factor of 50 was thought to be adequate,

and concerns were raised that the PAPR

32

could "mask" heat stress symptoms.

On January 22, 1996, a 53 4 DAC-hr air

sample was obtained during the job. The RWP was then revised (Rev. 3) to include

the use of PAPRs when contamination was expected to exceed

10 DAC-hrs.

10 CFR 20.1703, "Use of individual respiratory protective equipment," requires that

if respiratory protection equipment is used, the licensee

is to select respiratory

protective equipment that "provides a protection factor greater than the multiple by

which peak concentrations

of airborne radioactive materials in the work area are

expected to exceed the values specified in Appendix B to 10 CFR 20, Table 1,

column 3." In addition,

~.."ifthe exposure

is later found to be greater than

estimated, the corrected value must be used; if the exposure

is later found to be

less than estimated, the corrected value may be used."

Based on a review of RWP and radiological survey records, and discussions with HP

staff members, the inspector concluded that although air sample results exceeded

initial estimates, the application of engineering controls and selection of respiratory

equipment were reasonable

under the circumstances.

'I

The inspector also reviewed personal exposure records to evaluate the airborne

radioactivity exposure assessments.

Computer records showed that each of the

individuals that wore a filter respirator and was exposed to an airborne

concentration of 53.4 DAC-hrs received

a whole body count to evaluate uptake of

radioactive materials, and to assign internal dose.

One individual was assigned

an

internal dose of 3 mrem, two other individuals were assigned

an internal dose of 0

mrem.

The inspector noted that the licensee elected to use the whole body count

data for internal dose assessment.

Finally, the inspector reviewed the adequacy of airborne radioactivity sampling

practices for areas outside of the RWCU pump room.

Through interviews, the

inspector was informed that during Unit 1 RWCU pump work, in January 1996, a

continuous air monitor (CAM) was stationed on 749 foot elevation of the reactor

building.

However, the CAM was located in the eastern north-south hallway, and

not immediately adjacent to the entrance to the Unit 1 B RWCU pump room.

Licensee staff acknowledged that the location of the CAM was not ideal for

verifying that airborne radioactivity areas were limited to areas inside of the RWCU

pump rooms.

However, the staff explained that they had concluded that an

airborne radioactivity area did not exist outside of the entrance to the RWCU pump

room based on the following.

Negative pressure

air flow was maintained by plant ventilation, for the

majority of time, at the entrance to the RWCU pump rooms.

Throughout the

job, negative pressure

air flow was monitored with a hanging streamer.

Note:

Negative air pressure flow was lost for a period of time during non-

work activities.

Upon notification, the operations department performed an

air balance to restore negative air flow.

a 500 cubic feet per minute (CFM) HEPA was used inside the room to clean

airborne radioactivity as it was being generated.

33

High contamination

levels were not found in areas adjacent to the RWCU

pump room egress point.

Several thousand dpm/100 cm'as identified on

the step-off-pad at the egress point, and 1000 dpm/100 cm'as found on a

large area smear taken in clean areas surrounding the egress point.

Licensee

staff attributed this to contamination that was tracked out of the room,

rather than airborne radioactivity migration.

No individuals working in clean areas immediately outside of the RWCU

pump rooms, were found to have clothing contamination.

Based on this information, the inspector concluded the following.

The continuous air monitor located on the Unit 1 reactor building

749'levation,

eastern north-south hallway, was not positioned in a location to

allow immediate notification of an airborne radioactivity condition near the

entrance to the B RWCU pump room.

Considering the low contamination levels found at the egress point to the

Unit 1 749'B" RWCU pump room, it is not likely that an airborne

radioactivity area existed outside of the RWCU pump room entrance.

Based on a review of the ALARApost job review for RWP 1996-0045, and through

discussions with health physics supervision, the inspector was informed that

lessons learned during RWP 1996-0045 were planned to be incorporated into future

RWCU pump jobs planned for Unit 2.

c.

Conclusions

Based on this review, the inspector made the following conclusions.

Although the elimination of hot particle controls on RWP 1996-0045, Rev. 2,

showed

a lack of prudence,

no procedural violations or consequential

radiation exposures

were identified.

Although air sample results exceeded

the protection factor of the respirator

initially selected for RWCU pump work, the application of engineering

controls and selection of respiratory equipment were reasonable

under the

circumstances.

Internal dose assessments

and assignments,

following the use of respiratory

protection equipment with a protection factor less than the measured

airborne DAC-hr concentration,

were appropriate.

0

Pre-job ALARAand RWP planning for planned work in the Unit 1 B RWCU

pump room, which required the application of engineering controls including

use of water for dust suppression,

use of HEPA ventilation and containment

(e.g., maintenance

of negative pressure

air flow into the room) during RWCU

pump work, represented

a sufficient survey that was reasonable

under the

34

circumstances to conclude that an airborne radioactivity area would not exist

outside of the B RWCU pump room during pump work.

~

Considering the low contamination levels found at the egress point to the

Unit 1 749'B" RWCU pump room, it is not likely that an airborne

radioactivity area existed outside of the RWCU pump room entrance.

R8.3

Closed

Violation 50-387 388 96-04-02

The inspector performed

a review to evaluate licensee response to NRC Violation

50-387;388/96-04-02.

The inspector discussed

corrective actions taken with

various members of the health physics staff, and reviewed the following June 24,

1996, Reply to Notice of Violation 50-387/96-04-02 5 50-388/96-04-02.

The inspector verified that specific corrective actions described

in the licensee's

response

letter, dated June 24, 1996, were complete.

The inspector noted that

appropriate corrective actions were taken when radiological posting deficiencies

were identified, and based on licensee reviews, no unplann'ed radiation exposures

resulted from the radiological posting deficiencies.

This item is closed.

RBA

Closed

Unresolved Item 50-387.388 96-09-02

Note:

During NRC Inspection Nos. 50-387;388/96-09, the inspector noted that four

additional radiological posting deficiencies were identified in the station's condition

reporting system: one radiation area posting deficiency, and three high radiation

area posting/barricading

deficiencies.

An unresolved

item, URI 50-387;388/96-09-

02, was opened pending further NRC review of the licensee's review and evaluation

of these events.

The NRC evaluation of these deficiencies appears

as follows.

An unposted

radiation area was identified on July 22, 1996, at the entrance

to the Unit 2, 645'

residual heat removal (RHR) pump room.

The majority

of the room was controlled as a high radiation area.

However, a small area

inside the northeast door, leading to the high radiation area, with dose rates

as high as 12 mrem/h was not posted as a radiation area.

This condition

was corrected by placing a radiation area posting on the outer entrance door,

and documenting the occurrence

in the station condition reporting system

(CR-0956).

This failure constitutes

a violation of minor significance and is

being treated as a Non-Cited Violation, consistent with Section IV of the NRC

Enforcement Policy. This item is closed.

Upon further review, it was determined that the three high radiation area

posting/barricading

deficiencies had greater significance, and are considered

a violation of NRC requirements.

The review of this issue appears

in Section

R8.5 of this report.

Accordingly, this unresolved item is being

administratively closed.

35

R8.5

0 ened

Violation 50-387 388 96-10-03

"Radiolo ical Postin

Deficiencies"

During NRC Inspection Nos. 50-387;388/96-09, the inspector reviewed the

following condition reports that documented

deficiencies in barricading and posting

the access to high radiation areas.

CR 96-508

Unit 1 Turbine Building 676'. On May 5, 1996, the entrance to the D

Demin Room from the E Demin Room was not posted

as a high

radiation area, and had dose rates of 200 mrem/h.

CR 96-535

Unit 1 Turbine Building 676':

On May 11, 1996, the entrance to the

Steam Jet Air Ejector (SJAE) Room from the spare SJAE room was

not posted

as a high radiation area, and had dose rates of 1,200

mrem/h.

CR 96-1056

Unit 2 Reactor Building 779':

On July 31, 1996, an un-'posted

high

radiation area of 400 mrem/h was found originating from the HV-

24511B resin inlet valve.

An unresolved item, URI 50-387;388/96-09-02,

was opened

pending the licensee's

review and evaluation of these events.

During the followup review of these

condition reports, the inspector noted that an investigation was performed for each

of these events; safety assessments

concluded that each of these events had low

actual safety consequences;

causes

and causal factors were identified; corrective

actions and actions to prevent recurrence were identified; and a review of past

performance was performed.

These investigations were generally good.

However, the inspector noted that corrective actions implemented to address the

failure to post the access to the Unit 1 676'levation

D Demin Room from the E

Demin Room, were not effective in preventing the May 11, 1996, event in which

the entrance from the spare SJAE room was found blocked open with a hand truck.

In addition, the inspector noted that the July 31, 1996, event involving a high

radiation area found originating from the HV-24511 B valve was a repeat

occurrence.

Further, the inspector identified another condition report that

warranted review due to a similarity to these events.

Condition report number CR

96-1371 was initiated on September

6, 1996, when the door to the Unit 2 Turbine

Building 729'oisture separator room, a high radiation area with dose rates as high

as 800 mrem/h inside the room, was found propped open.

This effectively left the

access to the high radiation area un-barricaded

and un-posted.

Although a followup

review concluded that no unauthorized

entries were made into the room during the

time in which the door was left open and un-posted, this event provides an

indication that weaknesses

exist in the radiological posting and access control

program, and that corrective actions implemented to address

previous radiological

posting and barricading deficiencies, have not been effective in preventing

recurrence.

Due to the repetitive nature of these events, and the ineffectiveness of corrective

actions, collectively, these examples of radiological posting and barricading

36

deficiencies are considered

a violation of NRC requirements,

specifically, Technical Specification 6.12, "High Radiation Area," which requires each high radiation area

to be barricaded

and conspicuously

posted as a high radiation area.

{VIO50-

387;388/96-10-03)

S8

Miscellaneous Security and Safeguards

Issues

S8.1

U date

EA 95-250

Securit

Chillin

Effect

U date

EA 94-212

Securit

Chillin

Effect

The inspector reviewed the licensee's corrective actions for the events that led to the NRC

escalated

enforcement and Department of Labor actions.

The corrective actions committed

to by the licensee were in place in the Security Department including: management

reassignments,

mandatory management

and employee training, and improvements

in the

SSES Employee Concerns Program.

In addition, the inspector verified the

existence/conduct

of the Security Issues Team, which is a peer interaction process

intended to identify employee concerns to Security line management

as an alternative to

the PPSL Employee Concerns Program.

The inspector concluded that the implementation

of the corrective actions was acceptable.

The NRC will evaluate the effectiveness of these

measures

to prevent a chilling effect on raising safety concerns to management

during

future inspection and assessment

activities.

Y. !Vlana ement Meetin s

X1

UFSAR Review

A recent discovery of a licensee operating their facility in a manner contrary to the

Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a

special focused review that compares

plant practices, procedures

and/or parameters

to the UFSAR description.

While performing the inspections discussed

in this

report, the inspectors reviewed the applicable portions of the UFSAR that related to

the areas inspected.

The inspector reviewed selected sections of Chapters

12.1 - 12.5, "Radiation

Protection," of the Updated Final Safety Analysis Report (UFSAR), pertaining to

radiological controls, to evaluate the accuracy of the UFSAR regarding existing plant

conditions and practices.

No UFSAR discrepancies

were identified during this

review.

0

37

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on October 21, 1996.

The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No'roprietary information was identified.

INSPECTION PROCEDURES USED

IP 62707:

IP 71707:

IP 73051:

IP 83750:

IP 92700:

IP 92902:

Maintenance

Observation

Plant Operations

Inservice Inspection - Review of Program

Occupational Radiation Exposure

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup - Engineering

~Oened

50-387;388/96-1 0-01

50-387;388/96-1 0-02

50-387;388/96-1 0-03

Closed

ITEMS OPENED, CLOSED, AND DISCUSSED

URI

Weaknesses

during Unit 1 Restart

VIO

Control Rod Drive (CRDI Mechanism Replacement

VIO

Failure to post and barricade high radiation areas in

accordance

with Technical Specification 6.12

50-387/96-007-00

50-388/95-1 2-01

50-387/95-05-01

50-387;388/96-04-02

50-387;388/96-09-02

Discussed

LER

Loss of 4 Kv Bus

URI

HPCI On-line Maintenance

URI

Observation Of Activities On The Refueling Floor

VIO

High radiation area posting discrepancies

URI

Failure to implement procedural posting requirements

for a radiation area and high radiation areas

50-387;388/96-06-01

EA 95-250

EA 94-212

URI

Containment Bypass Leakage

Security Chilling Effect

Security Chilling Effect

LIST OF ACRONYMS USED

ALARA

CAM

CFM

CFR

CFR

CIV

CR

CRD

CRDM

CREOASS

DAC

dpm

EA

FSAR

gpm

HEPA

HP

HPCI

IR

ISES

LCO

LER

mR/h

mR

mrem/h

mrem

NCV

NOV

NRC

NRR

Ol

OPDRV

PAD

PAPR

PCC

PCM

PORC

RCIC

RHR

RWCU

RWP

SBGTS

scfh

SJAE

SRV

TCM

TIP

TS

UFSAR

URI

US

VIO

As Low As Is Reasonably Achievable

Continuous Air Monitor

Cubic Feet per Minute

Code of Federal Regulations

Code of Federal Regulations

Combined. Intermediate Valves

Condition Report

Control Rod Drive

Control Rod Drive Mechanism

Control Room Emergency Outside Air Supply System

Derived Air Concentration

disintegration per minute

Escalated Action

Final Safety Analysis Report

gallons per minute

High Efficiency Particulate Air

Health Physics

High Pressure

Coolant Injection

Inspection Report

Independent

Safety Evaluation Services

Limiting Condition of Operation

Licensee Event Report

milliRoentgen per hour

milliRoentgen

millirem per hour

millirem

Non-Cited Violation

Notice of Violation

Nuclear Regulatory Commission

NRC Office of Nuclear Reactor Regulation

Office of Investigations

Operations with the Potential for Draining the Reactor Vessel

Personal Alarming Dosimeter

Powered Air Purifying Respirator

power control center

Personnel

Contamination Monitor

Plant Operations Review Committee

Reactor Core Isolation Cooling

Residual Heat Removal

Reactor Water Cleanup

Radiation Work Permit

Standby Gas Treatment System

standard cubic foot/feet per hour

Steam Jet Air Ejector

Safety Relief Valve

Tool Contamination Monitor

Transverse

Incore Probe

Technical Specification

Updated Final Safety Analysis Report

Unresolved Item

Unit Supervisor

Violation