ML17158A870

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Insp Repts 50-387/95-17 & 50-388/95-17 on 950705-0805. Violations Noted.Major Areas Inspected:Operations, Maintenance,Surveillance,Engineering,Technical Support, Plant Support & Safety Assessment
ML17158A870
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 08/29/1995
From: Anderson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17158A868 List:
References
50-387-95-17, 50-388-95-17, NUDOCS 9509060251
Download: ML17158A870 (29)


See also: IR 05000387/1995017

Text

Inspection

Report Nos.

License

Nos.

Licensee:

Facility Name:

Inspection At:

Inspection

Conducted:

Inspectors:

UNITED STATES

NUCLEAR REGULATORY CONNISSION

REGION I

50-387/95-17;

50-388/95-17

NPF-14;

NPF-22

Pennsylvania

Power

and Light Company

2 North Ninth Street

Allentown, Pennsylvania

18101

Susquehanna

Steam Electric Station

Salem Township,

Pennsylvania

July 5,

1995

August 5,

1995

N. Banerjee,

Senior Resident

Inspector,

SSES

B. NcDermott, Resident

Inspector,

SSES

N. Blumberg, Project Engineer,

DRP

Approved By:

C.

erson,

C >e

Reactor Projects

Section

2B

841 f~

ate

95090602Sl

950829

PDR

ADOCK 05000387

Q

PDR

EXECUTIVE SUMMARY

Operations

Susquehanna

Inspection

Reports

50-387/95-17;

50-388/95-17

July 5,

1995

August 5,

1995

Alert and cognizant control

room operators

operated

both units in a safe

manner with shift supervision

providing good oversight (Section

2. 1).

Maintenance/Surveil'lance

In preparation for the Unit 2 7'" refueling outage,

new fuel inspection

activities were conducted

in a safe

manner with good supervision

and

engineering oversight (Section 3.3).

Engineering/Technical

Support

PP&L's evaluation of the visqueen

sheet retrieved

from the suppression

pool

during the Unit

1 outage provided

a reasonable

assessment

of its potential

impact on the Reactor

Core Isolation Cooling (RCIC) suction strainers

and gave

appropriate consideration to the potential for its transport to other areas

of

the suppression

pool

under dynamic conditions.

The evaluation

concluded that

RCIC operability was not impacted during previous operating cycles with the

visqueen

sheet in the pool Section

(Section 4. 1).

Plant Support

An unannounced,

after hour emergency

plan call-out exercise

revealed

problems

with PP&L's call-.out procedure

and the tele-notification system.

Although the

licensee's ability to respond in case of an actual

emergency

was maintained,

PP&L took the necessary

corrective actions

and re-performed the call-out

exercise with much improved results

(Section 5.3).

Safety Assessment/equality

Verification

During the Unit

1 refueling outage,

Operations

management

s decision not to

enter the Technical Specification

(TS) action called out by an emergency

diesel

generator test procedure is

a violation.

The safety significance of

the incident was minimal, and this action reflected operations

management's

poor judgement,

and

was not willful.

However, this violation is being cited,

because

the decision not to enter the required

TS action

was

made

by a highet

level

management

personnel,

and

a previous

Licensee

Event Report in 1994

discussed

the need to enter the TS action during the subject testing.

Plant

management

has

counseled

operations

management

and reinforced the need to

comply with plant TS.

(Section

6. 1).

A total of nine

LERs and one unresolved

item were reviewed

and closed

based

on

the inspectors

assessment

of the licensee's

corrective actions.

EXECUTIVE SUNNARY .

TABLE OF CONTENTS

.

TABLE OF CONTENTS

~

~ll

1.

SUNNARY OF FACILITY ACTIVITIES

2.

3.

PLANT OPERATIONS

2. 1

Plant Operations

Review ..

2.2

Use of Overtime

.

NAINTENANCE AND SURVEILLANCE

3. 1

Naintenance

Observations

3.2

Preventive

Naintenance of Core Spray

3.3

New Fuel Receipt Inspection

.

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Pump Notor

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4.

ENGINEERING

.

4.1

Evaluation Of Potential

RCIC Suction Stra incr

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Blocka

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5.

PLANT SUPPORT

.

5. 1

Radiological

and Chemistry Controls

.

5.2

Security

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5.3

Unannounced 'Off-Hour Exercise

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5

5

5

6.

SAFETY ASSESSNENT/EQUALITY VERIFICATION

~

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6. 1

Licensee

Event Report Review

6.2

Open Item Followup

6.3

10 CFR Part 21 Reports

7.

NANAGENENT AND EXIT NEETINGS

7. 1

Resident Exit and Periodic Neetings

.

7.2

Other

NRC Activities

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6

11

11

11llll

DETAILS

1.

SUNNARY OF FACILITY ACTIVITIES

Susquehanna

Unit 1 Suamary

Unit

1 was operated

at or near full rated thermal

power throughout this

inspection period.

minor power reductions

were made to support main turbine

valve testing, control rod pattern adjustment,

and to reduce

condenser

backpressure

resulting from extreme hot and humid weather.

Susquehanna

Unit 2 Summary

Unit 2 remained at power throughout the inspection period, with routine power

reductions for turbine valve testing

and control rod pattern adjustments.

Also, minor power reductions

were required to reduce

condenser

backpressure

on

several

unusually hot days.

On Friday July 21,

power was reduced to 58% for

planned maintenance

on the 'B'eactor recirculation motor-generator

set'nd

cleaning of the 'B'ain condenser

water box.

As of Sunday July 23,

power was

returned to 100%.

2.

PLANT OPERATIONS (71707,

92901,

93702)'.1

Plant Operations

Review

The inspectors routinely observed

the conduct of plant operations to verify

independently that the licensee

operated

the plant safely

and according to

station procedures

and regulatory requirements.

Control

room indications

and plant systems

were observed

independently

by NRC

inspectors

to verify that plant conditions were in compliance with station

operating

procedures

and Technical Specifications

(TS).

Control

room alarms

and bypass indication system

(BIS) warnings were routinely reviewed

and

discussed

with operators;

Operators

were cognizant of control

board

indications

and plant conditions.

Control

room and shift manning were in

accordance

with TS requirements..

The inspectors

conducted regular tours of the various plant areas

and

periodically reviewed logs

and records to ensure

compliance with station

procedures,

to determine if entries

were correctly made,

and to verify correct

communication of equipment status.

These records

included various operating

logs, turnover sheets,

blocking permits,

and bypass

logs.

The inspector

observed

plant housekeeping

controls including control

and storage of

flammable material

and other potential safety hazards.

Posting

and control of

radiation,

high

r adiation,

and contamination

areas

were appropriate.

\\

The inspectors

performed backshift

and deep backshift inspections

during the

period.

The deep backshift inspections

covered licensee activities between

10:00 p.m.

and 6:00 a.m.

on weekdays,

weekends,

and holidays.

The

inspection

procedure

from

NRC

manual

Chapter

2515

that

the

inspector

used

as guidance is parenthetically listed for each report section.

Based

on routine observations

in the Unit

1 and

2 control

room, the inspectors

concluded that alert

and cognizant operating

crews

had operated

the plant in a

safe manner following plant procedures,

with shift supervision providing good

oversight.

Plant housekeeping

was found acceptable.

2.2

Use of Overtime

The inspector

reviewed the licensee's

use of overtime by the unit staff who

perform safety-related

functions during the recently completed Unit

1 8'"

refueling outage.

The inspector

noted that in one case,

a Nuclear Systems

Engineer

had worked in excess

of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in a 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> time period.

The plant

technical specification section 6.2.2 limits the overtime to 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in any 48

hour period for unit staff who perform safety related function.

Upon

inspector's

questions,

the licensee clarified that this engineer's

use of

overtime did not involve jobs directly related to a nuclear safety function

(i.e., performing as

a test director for test of safety-related

equipment).

However, the licensee

prepared

a deviation form to document this overtime use.

Based

on

a sample review, the inspector

concluded the use of overtime during

the Unit

1 outage

was consistent with the requirements

of the plant Technical

Specification

(Section 6.2.2)

and licensee's

procedure

NDAP-00-650,

Conduct of

Site Support.

3.

MAINTENANCE AND SURVEILLANCE (62703,

61726,

92902)

3.1

Maintenance

Observations

The inspector

observed

and/or reviewed selected

maintenance activities to

evaluate

whether the work was conducted in accordance

with approved

procedures,

regulatory guides,

Technical Specifications,

and industry codes

or

standards.

The following items were considered,

as applicable,

during this

review:

Limiting Conditions for Operation were met while components

or

systems

were removed from service;

required administrative approvals

were

obtained prior to initiating the work; activities were accomplished

using

approved

procedures

and quality control hold points were established

where

required; functional testing

was performed prior to declaring the involved

component(s)

operable; activities were accomplished

by qualified personnel;

radiological controls were implemented; fire protection controls were imple-

mented;

and the equipment

was verified to be properly returned to service.

Maintenance

observations

and/or reviews included:

WA S15337,

Perform

5 Year

ESW

Pump Inspection,

August 3,

1995.

WA P45409; Unit 2 Core Spray

Pump 'B'ow Flow Check Valve Inspection,

August 1,

1995.

WA S50884,

Unit

1 'A'ain Transformer

Fan Cleaning, July 19,

1995.

WA P51032,

Negger

and Polarization Testing of the reactor

Core Spray

Pump 'D'otor, July 31,

1995.

Based

on sample inspection of the above maintenance,

the inspector

concluded

that the work was conducted

and completed appropriately,

with due concern for

plant safety

and procedures.

3.2

Preventive

Maintenance of Core Spray

Pump Motor

On July 31,

1995, the inspector

observed

WA P51032,

Megger

and Polarization

Testing of the reactor

Core Spray

Pump 'D'otor.

This test is an

18 month

periodic preventive maintenance

test performed for each core spray

pump.

The

inspector

observed

the test equipment readings

and noted that the test data

met acceptance criteria.

The test meter

was in calibration,

and

a quality

control

(gC) inspector witnessed

the test

as part of a

gC sampling'process

for

work on safety-related

equipment.

At the conclusion of the test, the

inspector

accompanied

the electrical

maintenance

supervisor in the clearing of

the tags,

the work authorization

(WA) documents,

and the equipment release

form (ERF).

The inspector

noted that the

WA and the tagging authorizations

are established

and cleared electronically.

The

ERF was cleared manually in

the control

room.

The overall maintenance activity was performed

satisfactorily.

3.3

New Fuel Receipt Inspection

On July 26,

1995, the inspector

observed

new fuel receipt inspection

activities

on the refueling floor in support of the upcoming Unit 2 refueling

outage.

The inspector

noted activities were performed following procedure

OP-

ORF-002,

New Fuel Receipt

and Inspection Activities, prerequisites

were

appropriately

checked,

good oversight of activities was performed

by the

Reactor

Engineer,

Maintenance

Supervisor

and the fuel vender representative.

The inspection

forms were duly completed,

and the operability of'ew fuel

vault criticality monitors were verified.

The inspector

concluded the

licensee

was performing the activity in an acceptable

manner with good

procedure

compliance

and supervision.

4.

ENGINEERING (71707,

37551,

92903)

4.1

Evaluation Of Potential

RCIC Suction Strainer Blockage

The Unit

1 suppression

pool inspection,

conducted during the Unit's 8'"

refueling outage,,

was to confirm the absence

of debris that could clog

emergency

core cooling system suction strainers.

During the inspection,

the

diver retrieved

a sheet of visqueen

(approximately 5'

5') found hanging from

the lower RCIC suction strainer bolts.

Condition Report

(CR)95-150 was

initiated to document this finding.

In the past,

visqueen

was

used to prevent

accidentally dropping debris into the suppression

pool,

and

has not been

used

after the 6th Unit

1 refueling outage.

Since

1989, the licensee

had

documented

debris that fell into the suppression

pool.

The licensee's

program

for foreign material

exclusion controls,

and suppression

pool inspection

were

reviewed in NRC combined inspection reports

50-387/94-22;

50-388/94-23

and 50-

387;388/95-08.

The

RCIC suppression

pool suction consists

of upper

and lower cone strainers

mounted vertically to

a "T" pipe, with each strainer

having

100% capacity.

Based

on the location of the visqueen, it was postulated that the

RCIC pump

suction could draw the visqueen'nto

the strainers

and block their flow.

At

the time of discovery,

the Technical Specifications

(TS) did not require

RCIC

to be operable

and the

CR did not address

system operability.

The visqueen

was

removed

from the suppression

pool

and

an evaluation for CR 95-150 was

subsequently

performed

by Nuclear Systems

Engineering.

The safety assessment

concluded that "...RCIC would have probably been able to perform its design

function with suction from the pool."

After reviewing this

CR evaluation,

the

inspectors

noted that it did not provide any detailed evaluation of the

visqueen's

potential

impact and that it's conclusion

was not definitive.

The

issue

was left as

an unresolved

item (URI 95-08-02)

pending the licensee's

documentation

and approval of an operability evaluation which addressed

the

ability of RCIC to perform its specified function.

A supplemental

operability. evaluation for CR 95-150 was written to address

the

potential

impact of the visqueen

on the

RCIC suction flowpath during previous

plant operation

when the system

was required to be operable.

This evaluation

compared

the as-found

geometry of the visqueen

sheet to the physical

configuration of the suction strainers

and associated

piping.

The licensee

concluded that the visqueen, if it had remained at the as-found location,

could have blocked

one of the strainers,

but would not have

had sufficient

additional material to block the remaining

100% capacity strainer.

The

analysis

also addressed

postulated

dislodging of the visqueen

sheet during a

LOCA and the potential for its impacting the

ECCS suction strainers.

In these

scenarios,

multiple strainers for redundant

ECCS loops are available to assure

reliability of the suppression

pool cooling water source.

Adequate

ECCS

capability would be maintained

assuming the visqueen

sheet

was transported to,

and blocked,

one

ECCS strainer.

The inspectors

reviewed the licensee's

documented

evaluation,

viewed

a video

tape of the diver's inspection,

and discussed

the issue with the responsible

system engineer.

The licensee's

evaluation provided

a reasonable

assessment

of the potential effects of the visqueen in the location it was found and gave

appropriate

consideration to the potential for transport to other areas of the

suppression

pool under dynamic conditions.

The inspectors

noted that the licensee's

CR operability determination

addressed

whether

TS required

RCIC to be operable,

but it did not address

the

system's ability to perform its intended function.

The subsequent

evaluation

by Nuclear System Engineering

di.d address

the function of RCIC but failed to

include any detailed evaluation of the visqueen sheet's

potential

impact or

a

definitive conclusion regarding operability.

The inspector considered

these

problems

a weakness

in the implementation of the

CR process

and operability

determination

procedure.

However, the inspector

concluded that the

supplemental

operability evaluation for CR 95-150 adequately

addressed

the

impact of the visqueen

sheet

on the operability of RCIC and

ECCS systems

during previous operating cycles.

This review closes

URI 95-08-02

(see

Section 6.2).

5

5.

PLANT SUPPORT (71750,

71707,

92904)

5.1

Radiological

and Chemistry Controls

During routine tours of both units, the inspectors

observed

the implementation

of selected

portions of PP&L's radiological controls

program to ensure:

the

utilization and compliance with radiological work permits

(RWPs); detailed

descriptions of radiological conditions;

and personnel

adherence

to

RWP

requirements.

The inspectors

observed

adequate

controls of access

to various

radiologically controlled areas

and use of personnel

monitors

and frisking

methods

upon exit from these

areas.

Posting

and control of radiation

areas,

contaminated

areas

and hot spots,

and labelling and control of containers

holding radioactive materials

were verified to be in accordance

with PP&L

procedures.

Health Physics technician control

and monitoring of these

activities was satisfactory.

Overall, .the inspector

observed

an acceptable

level of performance

and implementation of the radiological controls program.

5.2

Security (71707)

PP&L's implementation of the physical security program

was verified on a

periodic basis,

including the adequacy of staffing, entry control, alarm

stations,

and physical

boundaries.

The inspector

reviewed

access

and egr ess

controls, throughout the period.'o deficiencies

were found.

5.3

Unannounced

Off-Hour Exercise

During an unannounced,

after hour,

emergency

plan call-out exercise

on July

20,

1995, completion of off-site notification,

and the simulated

manning of ,

the emergency

response facilities took longer than expected.

The problem

involved delays in activating the beeper s,

as well" as, difficulties

experienced

by the

r esponders

in their ability to call-back through the tele-

notification system that was overloaded.

This resulted in the on-call

Emergency Director

(ED),

among others,

not being able to respond to tele-

notification.

The drill required the responders

to call-back to the tele-

notification system

and confirm their fitness for duty and provide an

estimated arrival time.

The drill scope did not require the responders

to

physically respond to their assigned

duty stations.

It was also noted that

completion of'otification to Luzerne County, took longer than

15 minutes;

and

several

responders

stopped their attempted call-in, after

a few attempts,

when

they found the tele-notification system to be jammed.

The licensee

performed

a review to determine root causes

and needed corrective

actions.

The licensee

concluded that although substantial

delay occurr ed in

the tele-notification process,

in case of a real event, timely manning of the

facilities would have happened.

The on-call

ED could not respond

back to the

tele-notification system but

a back up

ED personnel

was available

and in

contact with the plant.

The tele-notification system call-out sequence

was

noted

as

a major root cause of its overloading problem.

A problem was also

identified with the Luzerne County telephone,

which was corrected.

To correct the tele-notification system weakness,

the licensee

implemented

several

changes.

To facilitate manning of the emergency

response facilities,

the control

room communicator flow chart

was revised to require notification

to security, for initiation of the tele-notification system, prior to the

notification of the off-site agencies.

To prevent overloading of the

tele-notification system,

the call-out sequence

was revised to activate first

the Technical

Support Center

(TSC)

and the Interim Emergency Operations

Facility (IEOF),

and then the

EOF as required.

Also, the call-out priority

setting

was revised to include clerical positions at the very end of the call-

out.

A memo from the

EP manager clarified the response

procedure in case

problems are experienced

by the responders

while calling into the system.

With the above

changes

in place,

the licensee

ran another off-hour

tele-notification system call-out on July 26,

1995.

The changes

were

effective,

and improved response

was noted.

,Further refinement of the call-

out process

is being considered.

As the call-out drills did not exercise

physical

manning of the emergency

response facilities, another off-hour

unannounced dril.l to demonstrate this ability is being considered.

The inspector

r eviewed the July 20,

1995 and July 26,

1995 drill call-out

time-lines, the revised control

room communicator flow chart,

and hot box

material

provided to the control

room operators that described

the changes

made to the call-out sequence.

The inspector

observed

a shift supervisor

instructing his shift about the hot box material.

The inspector also reviewed

the July 26,

1995 remedial drill critique,

and discussed

the issues with the

emergency

planning personnel.

The inspector

concluded the changes

made to the

,call-out process

were timely and effective.

Licensee

management

provided

appropriate

emphasis

on understanding

and correcting the problem.

6.

SAFETY ASSESSNENT/EQUALITY VERIFICATION (92700)

6.1

Licensee

Event Report Review

The inspector

reviewed Licensee

Event Reports

(LERs) submitted to the

NRC

office to verify that details of the event were clearly reported,

including

the accuracy of the description of the cause

and the adequacy of corrective

action.

The inspector

considered

whether further information was required

from the licensee,

and whether generic implications were involved.

The following LERs were reviewed,

and the inspectors

concluded the licensee

met the reporting requirement,

LERs provided the needed

information,

and the

licensee's

corrective actions

were considered

adequate:

Unit 1

95-003-00

Unit 1 Shutdown

Due To Check Valve Surveillance Failure

On Narch 25,

1995, Unit

1 was shutdown from 100% power due to a failure of a

reactor

instrument line excess

flow check valve.

During the test,

the valve

failed to exhibit a significant decrease

in flow at the point of draining.

Excess

flow check valve testing is done just prior to unit shutdown for

refueling.

The

LCO was met since the unit was subsequently

shutdown for the

refueling outage.

During the outage, it was determined that the valve could

not be repaired;

and it was replaced.

The cause of'he failure has not yet

been determined;

however,

the valve has

been sent to the licensee's

laboratory

for analysis.

The licensee

determined that there were no generic

implications,

and the history of excess

flow check valves in the plant

indicates

a low probability for this type of failure.

95-005-00

Nissed Surveillance Test For 'D'mergency Diesel Generator

(EDG):

On Narch 29,

1995, during the Unit

1 Eighth Refueling Outage,

an engineering

review of past

emergency diesel

generator testing noted that

a hot restart

capability test of the 'D'DG had not been performed during the Unit 2 Fifth

refuelling outage

(September-November

1992).

The test

was subsequently

performed successfully

on January

2,

1994, during the Unit .1 Seventh

Refuelling Outage.

The apparent

cause

was that

a system test director

misunderstood

the test procedure requisite

and

assumed that

a hot restart test

performed

on the 'E'DG in Narch

1992 (during

a time period when the 'E'DG

was substituting for the 'D'DG) could be credited for the 'D'est.

Although the licensee

has

an automated surveillance authorization

(SA) system,

a procedural

misinterpretation still allowed the test to be overlooked.

18

month surveillance testing procedures

for the

EDGs have all been

changed to

clarify when the hot restart test must

be done.

This incident appears

to be

an isolated

occurrence

which was caused,

in part,

by the fact that the 'E'DG

can

be substituted for any of the other

EDGs.

The computer

generated

SA

system would normally preclude missing

a scheduled

surveillance.

This

incident of technical specification non-compliance

met the criterion,of

Section VII.B.1 in 10 CFR Part 2, Appendix C,

and is not being cited.

95-006-00

Result of Local Leak Rate Test of a Nain Steam Line Penetration

Exceeds Limit

On April 1,

1995, during the Unit

1 Eighth Refuelling Outage,

a main steam

line (NSL) penetration

local leak rate test through both the inboard

and

outboard main steam isolation valves

(NSIVs), indicated that the leakage of 53

standard

cubic feet per hour

(SCFH) exceeded

the required total

NSL

containment penetration

leakage of 46 SCFH.

The exact cause of the leakage of

,the valves

was not known; but the leakage

was apparently

caused

by some

corrosion

on the valve seats.

Stroking of the 'A', 'C'nd 'D'nboard

NSIVs

and the 'D'utboard

NSIV significantly reduced the leakage rate to 21

SCFH.

There have

been past incidents of NSIV leakage,

but the leakage did not affect

the integrated

containment

leak rate test.

The licensee

has submitted

a Technical Specification

change to raise the

leakage limits to 100

SCFH for any one NSIV and to 300

SCFH for all NSIVs

combined.

This request is currently undet

review by the

NRC.

Based

on the

licensee's

analysis

for offsite and control

room dose,

the leakage

was of low

safety significance.

If Technical Specification is approved,

the current

"as

found" leakage during tests

should normally be below the required limits.

(Post inspection note: the

NRC,

on August 18,

1995,

approved this technical

specification change).

e.

8

95-007-00

Unplanned

ESF Actuation of RPS

Due to Spurious Instrumentation

Upscale Signal

This

LER documents initiation of a scram signal during the recently completed

Unit I refueling outage,

while the

RPS was in the non-coincident trip mode,

due to spupious

intermediate

range neutron monitor (IRN) upscale signals.

During the time, control

room operators

were performing control rod stroke

'time and friction testing,

and in accordance

with the plant procedure shorting

links were removed to initiate a full scram signal

from the trip of any one of

the two RPS channels.

Spurious signal spiking of the

IRNs has

been

observed

on numerous

occasions

during refueling outages

when neutron flux levels are low and the

IRNs were at

their lower ranges.

At these

ranges

instrumentation is more susceptible

to

noise

due to high system gain.

The licensee

conducted

an investigation to

identify the source of the noise,

but a source

was not identified.

However,

one of the two IRNs associated

with the event

had

a lower than desirable

detector resistance

to ground,

and the licensee

believed that had contributed

to the event.

The licensee

plans to replace the degraded

detector during the

next refueling outage.

The licensee is also evaluating the requirement of

removing the shorting links to support control rod testing

and intends to

pursue it as

a part of their technical specification

improvement.

The inspector

concluded the safety significance of the event

was minimal.

95-008-00

Unplanned

ESF Actuation 'B'mergency Diesel Generator

Automatic

Start

On April 27,

1995,

an unplanned

automatic start of the 'B'mergency Diesel

Generator

(EDG) occurred

due to physical

bumping of a

125V DC circuit breaker.

The circuit breaker,

located, inside the diesel

generator

control

panel

was

found in the open position.

Due to the loss of the

125Y

DC control circuit,

, although it started,

the 'B'DG would not have properly loaded

had it been

called

upon to do so.

The other three

EDGs were operable.

The breaker

was

subsequently

reclosed,

and the

EDG successfully tested.

The breaker

was

replaced with a breaker

from the

same manufacturer/model

number.

The licensee

plans to test the removed breaker at

a future date.

The licensee

indicated the breakers,

provided by Heineman,

are not used in any

other safety-related

applications in the plant.

The licensee

considered

the

incident isolated

and their review with the Cooper

Bessemer

Owners

Group did

not identify any generic concern with the breaker.

Regarding physical

bumping

of the breaker,

a task team at Susquehanna

is currently reviewing various

known incidents of human performance errors,

and developing

ways to improve

human performance.

Unit 2

95-001-00

Operation at Power with an Inoperable

Excore Neutron Flux Monitor

On January

30,

1995, while Unit 2 was at

100% power, the Excore Neutron Flux

Channel 'B'og power range indicator failed and

was reading upscale.

The

condition could not be corrected.

A notice of enforcement discretion

(NOED)

was obtained

from the

NRC on February 6,

1995, to allow continued plant

operation.

Operation in this condition was allowed until the next refueling

outage

scheduled to begin in September

1995.

Technical

issues

and licensee

actions

concerning this

LER were discussed

in NRC Inspection

Report 95-02.

95-002-00

Unplanned Engineering Safety Feature

(ESF) Actuation Due to

Operator Switching Error

On February 8,

1995, with Unit 2 at

100% power,

an unplanned

ESF actuation

occurred

when

a normally open primary containment isolation valve for the

Traversing Incore Probe

(TIP) Indexer automatically closed following the de-

energization of a

120 volt power supply circuit.

The cause of the problem was

operator error in that during

a routine work evolution

a blocking tag was

applied to a number

13 breaker

instead of the called for number

3 breaker

.

The error was discovered'bout

three

hours later by an electrician

who was

verifying electrical

blocking for a scheduled

maintenance activity.

Status indication of six pieces of equipment

was lost,

and

an

ESF actuation

occurred

when normally open primary containment isolation valve for TIP

Indexer automatically closed following de-energization

of the power supply.

There were no alarms in the Control

Room, but status indication for the valve,

which is located

on

a back panel,

was lost.

This loss of indication 'was not

noticed

by Control

Room operators

during

a shift turnover panel

walkdown.

Corrective action included retraining of nuclear plant operators

and control

room operators

on the weaknesses

that caused this event.

Regarding the

human

performance

aspect of the event,

a licensee task team is currently reviewing

the

human performance error events to develop comprehensive

corrective

actions.

95-006-00

Condition Prohibited by the Plant's Technical Specification

(LCO 3.0.3)

During the recently completed Unit

1 refueling outage,

the licensee

performed

an

18 month surveillance of the Emergency

Diesel

Generators

(EDG) and

Engineered

Safeguards

System

(ESS)

Buses

on Loss of Offsite Power with a

LOCA.

This test is performed

on each division of EDGs at

a time, thus affecting two

EDGs

and two ESS buses.

During the testing, the auto-close

permissive relays

for the primary and feeder

breakers

to the subject

ESS buses

are de-energized,

and undervoltage start signals to the respective

EDGs are bypassed.

This

ensures verification of automatic start of the subject

EDGs upon

a

LOCA signal

and subsequent

sequential

loading of safety-related

equipment

on the

respective

ESS buses.

Since the

EDGs are shared

between the two units,

and

the Unit

1 buses

carry loads

common to both units, entry into a Unit 2

technical specification

(TS) limiting condition of operation

(LCO) is required

when any of these Unit

1

ESS buses

are not energized.

By virtue of removing

10

the main and alternate

feeder auto-closing features

from two of the Unit

1

ESS

buses,

these

buses

are considered

de-energized.

As the Unit 2 TS does not

address

de-energizing

two

ESS

buses

the test procedure specifies entry into

LCO 3.0.3 for Unit 2.

LCO 3.0.3 requires that within one hour actions

be

taken to enter hot shutdown in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

and cold shutdown in following 24

hours.

During Division I testing, the licensee

entered into

LCO 3.0.3,

as it did

during the previous

performance of this

18 month surveillance.

But, during

Division II testing,

operations

management

made

a determination that such

an

entry was not required.

This decision

was contrary to the guidance

provided

in the licensee's

test procedure

and Technical Specification

(TS)

Interpretation

(TSI) document

No. 2-88-001.

Also, during the previous Unit

1

outage the licensee

determined that entry into

LCO 3.0.3

was necessary

during

performance of the subject test,

and

an

LER (94-001)

documented this entry.

The operations

management

was counseled

by plant management,

and is reviewing

the TSI 2-88-001 with the licensed

operators

regarding the need to enter

LCO 3.0.3 during performance of this test.

The licensee is currently preparing

a

TS change for submittal to the

NRC that will preclude

need for entry into

LCO 3.0.3 during the testing.

The

NRC inspector

was informed that,

pending

a TS

change, this

LCO will be entered

during future performance of the test.

The inspector

reviewed the

LER, the test procedure

steps

and

had discussions

with operations

management,

the test engineer

and the licensing engineers.

The inspector

concluded that the actual safety significance of not entering

LCO 3.0.3

was minimal,

as the respective

buses

were continually energized

during the test except for 10 seconds

from bus de-energization

to re-

energization

by the.EDGs.

As the main and al'ternate

feeder

breaker auto-

closure protective features

were

bypassed, if an

EDG failed to re-energize

the

bus,

manual

action would have

been necessary

to remove the bypasses

and

energize

the bus.

The test procedure

required positioning nuclear

plant

operators

at the breaker locations,

hence the needed

actions

can

be taken

promptly.

The inspector

concluded that the licensee's

decision not to enter

LCO 3.0.3 in this case

was

a violation of plant technical specifications.

This violation is being cited,

because

the decision

was

made

by a higher level

management

personnel,

and the need to enter the technical specification

required action during the subject testing

was previously identified by the

licensee,

as reflected in LER 94-001.

(VIO 50-388/95-17-01)

95-007-00

Local Leak Rate Testing Not Performed

on Two Electrical

Penetrations.

Since Original Construction

On February 27,

1995, work planning reviews to support Unit 2 containment

local leak rate testing

(LLRT), identified that two electrical penetrations

used for the Excore Neutron Nonitoring System

had not been local leak rate

tested

since original construction in 1983.

The penetrations

had

been local

leak rate tested

during pre-operational

testing;

however,

through

an

oversight,

the need to leak rate test these penetrations

was not transferred

to licensee

documents.

0

11

As a corrective action, the licensee

reviewed all plans

and documents

and

performed

a walkdown of the containment penetrations

to ensure that

LLRTs have

been performed.

No further discrepancies

were found.

27 penetrations,

which

are located in inaccessible

or high radiation areas, will be visually verified

to be spare penetrations,

and

do not require

LLRT, during the upcoming Unit 2

Seventh Refuelling Outage starting, in September

1995.

In addition, the

licensee

performed

an

LLRT on the two penetrations

and both passed.

6.2

Open Item Followup

(Closed)

URI 50-387;388/95-08-02,

RCIC Suppression

Pool Suction Blockage

This unresolved

item is closed

based

on the inspector's

review documented

in

section 4. 1 of this report.

6.3.

10. CFR Part

21 Reports

Ethylene Glycol Fill Liquid in ITT Barton Differential Pressure

(D/P)

Indicators

and Differential Pressure

Indicating Switches

An ITT Barton Industry advisory dated

March 13,

1995, stated that for certain

Model

Gages filled with ethylene glycol, the ethylene glycol may disassociate

in radiation fields in excess of lE6 RADs.

The licensee

reviewed its environmental qualification (Eg) data

base for all

ITT Barton D/P switches regardless

of filling.

Only two D/P switches

were

found to have the potential for being exposed to fields in excess of lEG RADs.

These switches

are used for initial operation of the

HPCI system.

Based

on

a

review of the environmental profile of the areas

where these

switches

are

located,

the licensee

concluded. that the switches

would no longer

be needed

when the radiation fields ultimately exceeded

those in the advisory.

Based

on

this review, the licensee

determined that there is not

a problem at SSES.

The review by the licensee for this issue

was both prompt and comprehensive.

7.

MANAGEMENT AND EXIT MEETINGS (71707)

7.1

Resident Exit and Periodic Meetings

The inspector

discussed

the findings of this inspection with PPKL station

management

throughout the inspection period to ensure timely communication of

emerging concerns.

At the conclusion of the reporting period, the resident

inspection staff conducted

an exit meeting summarizing the preliminat y

findings of this inspection.

Based

on

NRC Region I review of this report

and

discussions

held with licensee

representatives, it was determined that this

report does not contain information subject to 10'FR 2.790 restrictions.

7.2

Other

NRC Activities

The following region based

NRC inspection activities/management

visits took

place during this period:

Dates

12

~Re ort No.

Ins ection Procedure

Lead Ins ector

July 24 - 28

July 24 - 28

July

18 5 27

95-17

95-19

64704, Fire Protection

84750, Effluent

SALP Board Nembers Visit

Harrison

Jang

J'..

4