ML17159A032
| ML17159A032 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 10/30/1997 |
| From: | Anderson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17159A030 | List: |
| References | |
| 50-387-97-07, 50-387-97-7, 50-388-97-07, 50-388-97-7, NUDOCS 9711070080 | |
| Download: ML17159A032 (54) | |
See also: IR 05000387/1997007
Text
e
U. S. NUCLEAR REGULATORY COMMISSION
REGION
I
Docket Nos:
License Nos:
50-387, 50-388
Report No.
50-387/97-07, 50-388/97-07
Licensee:
Pennsylvania Power and Light Company (PP&L)
2 North Ninth Street
Allentown, Pennsylvania
19101
Facility:
Susquehanna
Steam Electric Station
Location:
P.O. Box 35
Berwick, PA 18603-0035
Dates:
August 17, 1997 through October 20, 1997
Inspectors:
Approved by:
K. Jenison, Senior Resident Inspector
B. McDermott, Resident Inspector
J. Richmond, Resident Inspector
Clifford J. Anderson, Chief
Projects Branch 4
Division of Reactor Projects
V7if070080 9'71030
nOOCK OSOaOSa7'
0
EXECUTIVE SUMMARY
Susquehanna
Steam Electric Station (SSES), Units 1 5 2
NRC Inspection Report 50-387/97-07, 50-388/97-07
This inspection included aspects of Pennsylvania Power and Light Company's (PPSL's)
operations, maintenance,
engineering and plant support at SSES.
The report covers a nine
week period of resident inspection.
~Oerations
PPSL management
conservatively opted to shut down Unit 2 in response to an
increasing trend of unidentified reactor coolant system leakage before reaching
Technical Specification (TS) limits. Good management
involvement was observed
during preparation for the shutdown and an orderly shutdown was conducted with
no significant challenges to the operators.
An inspector follow-up item was opened
to track the licensee's root cause investigation of the equipment failure.
(Section
01.1)
A reactor feedwater pump (RFP) minimum flow control valve failed open resulting in
a reactor water level induced transient.
The Plant Control Operator (PCO) reduced
power to approximately 68%, reactor water level was recovered,
and the unit was
returned to a steady state condition.
PCO actions were conservative
and in
accordance with unit procedures.
The licensee initiated an event review team (ERT)
to determine the root cause of the transient.
The cause of the equipment failure
and the results of the ERT investigation will be reviewed as an inspector follow-up
item. (section 01.2)
Interviews were conducted with licensed and non-licensed operators to assess
the
implementation of SSES Operations department procedure OI-AD-016, Operator
Rounds.
Based on these interviews, the inspectors determined that portions of
procedure sections 4.2 through 4.5 were routinely delayed, amended or missed
during periods of high activity. This issue was discussed with licensee management
on three occasions.
The licensee made changes to the procedure to ensure that the
procedure was clear and allowed shift supervision the flexibilityto delay or amend
the requirements for general equipment inspections in the subject procedure steps.
The licensee's
immediate corrective actions were adequate
and were completed
prior to the end of the inspection period.
The failure to follow procedure Ol-AD-016
as written during previous operator rounds was a violation of TS 6.8.1.
(section
01.3)
The PCOs responded well to those alarmed conditions requiring actions.
PCOs were
able to describe the reasons for their actions and discuss the impact of their actions
upon the units.
PCO actions were determined to be conservative and in accordance
with established
plant procedures.
(section 04.1)
The resolution of several issues by the PPSL Corrective Action Team (CAT) was
direct, safety oriented, and conservative.
(section 07.1)
Executive Summary
Maintenance
The work authorization (WA) activities observed during this inspection period were,
in general, well performed.
The WAs described
and controlled maintenance
activities with adequate,
but in some cases general, procedures.
The maintenance
activities were implemented by well trained and experienced maintenance
technicians,
and resulted in equipment being returned to service in good conditior .
(section M1.1)
SSES surveillance activities, observed during this inspection period, were well
performed, described and controlled by detailed SSES procedures,
and performed by
well trained, experienced
and capable technicians/operators.
(section M1.2)
The maintenance task certification matrix and its implementation were adequate to
control the assignment of qualified workers to safety related
maintenance
activities.
No violation of NRC requirements was identified. (section M1.3)
The licensee's corrective actions in response to an interrupted cool down of the "C"
(EDG) were adequate.
The interrupted cool down did
not affect the operability of the EDG. (section M2.1)
PPRL requested
enforcement discretion for TS requirements concerning
a failed
acoustic position indicator for the "S" Safety Relief Valve.
PPSL requested
the
enforcement discretion to avoid an undesirable transient as the result of forcing
compliance with a license condition. The NRC approved PPRL's request after
determining the action involved minimal or no safety impact and had no adverse
radiological impact on public health and safety.
(section M2.2)
PPRL allowed maintenance work to proceed on the "A" Standby Liquid Control
(SBLC) pump nitrogen accumulator without evaluating whether the activity would
affect operability. After questions regarding operability impact were raised by the
NRC, an initial operability determination by the Shift Technical Advisor was weak
because lt did not address known technical issues with the potential to affect
operability.
The failure to provide adequate
procedures for control of maintenance
on safety related equipment is a violation of TSs.
(section M3.1)
'I
Corrective actions for a safety related check valve deficiency, identified in 1994, did
not address generic implications.
In 1996, the same condition was identified on a
different valve and, in this case, the planned actions to prevent recurrence were
appropriate.
However, the administrative process to implement and track these
actions was not initiated. These two corrective action problems are considered
a
violation of minor significance because this had no impact on safety.
(section
M7.1)
Executive Summary
EncnineerinE
~
The erosion control program portion of engineering corrective actions for an
indicated high level in a reactor core isolation cooling (RCIC) drain pot was
determined to be outstanding.
(section E2.1)
~
The engineering corrective actions for problems with the Unit 1 RCIC drain pot level
switch were not timely. This allowed continuous degradation of the drain line and a
continuous alarmed condition for over ten months after it caused
a forced
shutdown.
A modification to replace the drain pot level switch was completed and
has been effective in restoring the normal operation of the RCIC system.
(section
E2.1)
In February 1997, PP&L identified that the "A" Control Structure (CS) chiller would
not automatically start as designed
and took immediate actions to correct. the
problem.
However, PP&L initiallyfailed to recognize this condition as outside the
plant's design basis, as described
in the Final Safety Analysis Report. After
identification by the NRC, PP&L initiated a Condition Report, determined the
condition was reportable, and submitted a Licensee Event Report as required.
Corrective actions for both the technical problem and the failure to recognize the
condition outside the design basis were implemented by PP&L.
In this case, the
failure to report a condition outside the design basis within 30 days of discovery is
characterized
as a non-cited violation. (section E4.1)
The initial operability determination for the Unit 2 High Pressure
Coolant Injection
(HPCI) overspeed trip assembly problem was weak.
Nuclear System Engineering
personnel overlooked the potential impact on the HPCI injection valve and how this
impact could affect the response time to rated flow. PP&L management
made a
conservative decision to declare HPCI inoperable, pending further evaluation.
A
subsequent
revision of the operability determination provided a good basis for
operability. Significant licensee attention was focused on resolution of the problem
and the overspeed trip assembly has performed acceptably since the corrective
maintenance.
(section E4.2)
PP&L failed to perform a 10 CFR 50.59 safety evaluation prior to opening a plant
equipment hatch assumed to be closed by the tornado design basis analysis.
This
condition existed for an extended period before identification by the NRC.
Subsequently,
plant equipment hatches have been verified to be in the condition
assumed
by the tornado analysis (shut) and are now being administratively
controlled.
PP&L's evaluation to determine whether an unreviewed safety question
existed with the hatch open is expected in January 1998 and will be reviewed to
determine the safety significance of this violation.
In the interim, this item is being
tracked as an unresolved item.
(section E8.1)
A review of the SSES responses
to 10 CFR 50.63, Station Blackout (SBO) rule was
conducted.
The licensee installed an auxiliary diesel power source to increase the
SBO coping duration of its 125 Vdc batteries from approximately 5-hours to greater
than 8-hours.
The NRC safety evaluation report concluded that SSES must meet a
0
Executive Summary
4-hour coping duration.
Therefore, the inspectors concluded that there was no
current regulatory requirement for the licensee to maintain the auxiliary power
source.
(section E8.2)
PPSL failed to perform a 10 CFR 50.59 safety evaluation prior to placing a floating
service platform on the spray pond that serves as the ultimate heat sink for both
SSES units. This condition existed for an extended period before identification by
the NRC.
PPRL has yet to perform an evaluation to determine whether an
unreviewed safety question existed with the platform on the spray pond.
Subsequently,
the spray pond was verified to be in the condition assumed
by the
Final Safety Analysis (the platform was removed).
Analysis of the spray pond
design basis and evaluation of the potential USQ will be reviewed with the response
to this violation. (section E8.3)
I. Operations
01
04
07
08
TABLE OF CONTENTS
Conduct of Operations .............
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1
01.1
Unit 2 Shutdown Due to Increasing Unidentified Drywell Leakage .,
1
01.2
Operator Response to a Feedwater Level Transient ...
~ .. ~....
~ 3
01.3
Nuclear Plant Operator (NPO) Performance
~
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Operator Knowledge and Performance ......,.... ~............
~ .. 5
04.1
Operator Response
to Operating Occurrences ..
~ .., ~... ~...
~ . 5
Quality Assurance
in Operations ....
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6
07.1
Corrective Action Team (CAT) Support of Plant Operations ...... 6
Miscellaneous Operations Issues ~...
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08.1
Review of Licensee Event Reports
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08.2
Review of NRC Open Items
.
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I. Maintenance
I
. 10
M1
M3
Conduct of Maintenance....................................
10
M1.1
Preplanned Maintenance ActivityReview ..................
10
M1.2
Preplanned
Surveillance ActivityReview...... ~... ~.... ~...
11
M1.3
Maintenance Technician Task Certification ..
~ ~.............
12
Maintenance and Material Condition of Facilities and Equipment .......
13
M2.1
Trip of the "C" Emergency Diesel Generator
(EDG) During Surveillance
Testing..........................................
13
M2.2
Unit 1 "S" Safety Relief Valve (SRV) Acoustic Position Indicator
(Acoustic Monitor) Failure
.
~ .. ~... ~...
~ ~...............
14
Maintenance Procedures
and Documentation ........ ~...........
1.5
M3.1
Release of Unit 1 Standby Liquid Control (SBLC) Accumulator Work
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Quality Assurance
in Maintenance.................. ~.........
17
M7.1
Unit 1 RHR Pump "A" Recirculation Check Valve Inspection ~.... 17
M7.2
Condition Report (CR) Support for Maintenance Activities ......
18
III. Engineering................ ~..... ~.............,.......,
..
~ ..
. 19
E2
E4
E8
Engineering Support of Facilities and Equipment
E2.1
Reactor Core Isolation Cooling (RCIC) Drain Pot Level Switch ..
Engineering Staff Knowledge and Performance
E4.1
Control Structure Chiller Automatic Start Capability........
~
E4.2
High Pressure
Coolant Injection (HPCI) Operability Determination
Miscellaneous Engineering Issues...............
~ .. ~........
E8.1
Unit 2 Reactor Building Truck Bay Hatch
E8.2
Station Blackout Design Basis ........... ~....... ~....
E8.3
Floating Service Platform on Safety Related Spray Pond
. ~....
.. 19
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. 20
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. 22
.. 24
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. 27
V. Plant Support ........
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I
F2
Status of Fire Protection Program
F2.1
Control Room CO, Fire Protection System .. ~...
R7
Radiological protection and Chemistry (RPC) Controls
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VI
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R7.1
Health Physics Frisking, Problems and Corrective Actions ....... 28
V. Management Meetings........................
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Exit Meeting Summary .......................
ITEMS OPENED, CLOSED, AND DISCUSSED
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o 30
LIST OF ACRONYMS USED................
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~ 3 1
Re ort Details
Summar
of Plant Status
Unit 1 began the inspection report period at 100% power.
Temporary power reductions
were made for planned activities including main turbine valve testing,
sequence
exchange,
a condenser water box leak investigation, and control rod scram time
testing.
An unplanned power reduction was necessary
as a result of a reactor feedwater
pump minimum flow valve that failed open'on September
1, 1997. At the end of the
report period, Unit
1 was at 100% power.
Unit 2 began the
inspection report period at 100% power,
An unplanned shutdown was
performed on September
16, 1997, in response to an increasing trend of unidentified
reactor coolant leakage.
After repairs were made to a cracked valve bonnet vent line, the
unit was returned to operation on September 24, 1997.
Other temporary planned power
reductions were made to support a control rod sequence
exchange, control rod scram time
testing, and main turbine valve testing.
At the end of the report period, Unit 2 was at
100% power.
I. 0 erations
01
Conduct of Operations
01.1
Unit 2 Shutdown Due to lncreasin
Unidentified Dr well Leaka
e
a.
Ins ection Sco
e 71707
On September
12, 1997, Plant Control Operators
(PCOs) identified an increasing
trend on both divisions of the containment radiation monitor and a corresponding
increase in the unidentified leakage collected in the "B" Containment Sump (CR 97-
3022). The inspectors reviewed the licensee's
actions in response to these
indications of a leak inside containment.
b.
Observations
and Findin s
The Technical Specification (TS) 3.4.3.2 lim!tfor unidentified reactor coolant
system leakage is 5 gpm, or an increase of 2 gpm in any 24-hour period.
I'ollowingthe Spring 1997 refueling outage, the Unit 2 unidentified leakage rate
was typically 0.04 gpm or less.
On September
12, 1997, the unidentified leakage
rate increased to approximately 0.80 gpm and then stabilized for several days.
Chemistry samples of the containment sump indicated that the leak was from
reactor coolant, e.g. the liquid portion of the primary system, rather than a steam
piping leak.
PPSL management
began planning for a shutdown on September
19,
1997 to minimize the radiological impacts during the next refueling outage.
However, on September
16, the leakage rate took a second step increase, to an
average of approximately 2.0 gpm.
PPRL management
decided to initiate an orderly plant shutdown on September 16,
1997, based on the increasing leakage rate.
The inspectors observed that
0
.2
Operations management's
expectations for control of the shutdown were clearly
articulated at the pre-activity briefing. As of September
17, 1997, Unit 2 was in
the Cold Shutdown condition for investigation of the leak and to make repairs.
The
inspectors considered
PP&L's decision to shut down ahead of schedule because
of
the increasing leakage trend, and before reaching TS limits, a conservative measure.
After the unit was placed in Cold Shutdown, PP&L determined the leak was from a
0.75 inch bonnet vent line off the "B" Reactor Recirculation Pump discharge valve.
A weld on the vent line was found to have a through-wall crack, 180 degrees
around its circumference.
PP&L's preliminary finding was that the vent line had not
been properly installed during the Spring 1997 outage'and that vibration caused
a
weld to crack.
PP&L's review of vibration test results from the Unit 2 seventh refueling outage,
and work authorizations (WAs) performed since that time, did not identify other
similar maintenance
circumstances.
In addition, inspections of lines similar to the
one that failed were performed to identify similar configurations with the potential
for fatigue failure and no evidence of such conditions were found.
PP&L concluded
the Unit 1 systems would be unaffected by the implications of this incident because
Unit 1 containment experiences
less vibration than Unit 2 and because tests of
vibration sensitive piping during the Unit 1 eighth refueling outage were acceptable.
Based on the root cause investigations initial findings, the maintenance
error which
led to this failure was considered
an isolated case.
The failed vent line and its associated
isolation valves were not used by PP&L and
therefore they were removed during the forced outage through a formal plant
modification. A start up Plant Operations Review Committee (PORC) meeting was
conducted on September 21, 1997.
The shutdown open item list was reviewed
and each item was dispositioned by the committee.
The inspectors observed that
the committee asked thorough and probing questions regarding the resolution of
technical issues.
PP&L management
acknowledged
a weakness
exists in the
number of ways the plant can be modified that do not use the same level of control
required In the formal modification process.
Programs other than the modification
process that can change plant components,
or equipment configuration, include
Replacement Item Equivalents, maintenance
repairs or use-as-is,
Bypasses, setpoint
changes,
and several others.
Nuclear System Engineering (NSE) management
is
evaluating this weakness
and is developing
a corrective action plan.
The bonnet vent line failure is the first example of an equipment failure that
necessitated
an unplanned operational transient during this inspection period.
An
inspector follow-up item (IFI) will be opened to track this issue for future NRC
review of the licensee's root cause investigation and corrective actions for this
equipment failure. A second equipment failure during this period is discussed
in
Section 01.2 of this report and will also be tracked under this item.
(IFI 50-
387,388/97-07-01 a)
c.
Conclusions
PPSL management
conservatively opted to shut down Unit 2 in response to an
increasing trend of unidentified reactor coolant system leakage before reaching TS
limits. Good management
involvement was observed during preparation for the
shutdown and an orderly shutdown was conducted with no significant challenges to
the operators.
An inspector follow-up item was opened to track the.licensee's
root
cause investigation of the equipment failure.
01.2
0 erator Res
onse to a Feedwater Level Transient
a.
Ins ection Sco
e 71707
On September
1, 1997, the Unit 1 "B" Reactor Feedwater Pump (RFP) minimum
flow control valve failed open.
This control valve failure resulted in a reactor water
level transient.
The inspectors reviewed the licensee's
response to this transient.
b.
Observations
and Findin s
On September
1, 1997, an RFP minimum flow control valve failed open directing
approximately 6000 gpm from the discharge of the "B" RFP to the main condenser
hotwell. Because of the flow being recirculated to the hotwell, instead of being
supplied to the reactor vessel, steam flow exceeded feedwater flow and reactor
water level began to decrease.
The Plant Control Operator (PCO) reduced power to
approximately 68%, control of reactor water level was recovered,
and the unit was
returned to a steady state condition.
The inspectors reviewed the actions of the
control room operators and determined that their actions were conservative
and in
accordance with unit procedures.
The licensee initiated a WA to repair the control
valve and established
an Event Review Team (ERT) to review the root cause of the
The inspectors considered the feedwater control valve failure a second example of
an equipment failure that caused
an unplanned operational transient during this
inspection period.
An IFI item will be opened to track this issue for review of the
licensee's root cause investigation and corrective actions.
(IFI 50-
387,388/97-07-01 b)
C.
Conclusions
A reactor feedwater pump (RFP) minimum flow control valve failed open resulting in
a reactor water level induced transient.
The PCO reduced power to approximately
68%, reactor water level was recovered,
and the unit was returned to a steady
state condition.
PCO actions were conservative and in accordance with unit
procedures.
The licensee initiated an Event Review Team (ERT) to review the root
cause of the transient.
The cause of the equipment failure and the results of the
ERT investigation will be reviewed as an inspector follow-up item.
I,
0
o~s
Nuclear Plant 0 erator
Performance
Ins ection Sco
e 71707
On October 9, 1997, the inspectors determined that certain portions of NPO rounds
as described
in Operations department procedure Ol-AD-016 were not being
performed in a consistent and complete manner.
A review of the licensee's
corrective actions for this issue was performed.
b.
Observations
and Findin s
Based on interviews with five NPOs and ten licensed operators, the inspectors
determined that the licensee was not fully implementing Operations department
procedure OI-AD-016, Operator Rounds.
The inspectors determined that the
required check sheet data, including TS surveillances, were being adequately taken
during operator rounds.
However, additional Ol-AD-016 general and routine
required actions were not always performed when other plant activities were
deemed more appropriate by the Unit Supervisor and/or the Assistant Unit
Supervisor.
The flexibilityto omit certain general visual inspections (GVls) was not
addressed
in Ol-AD-016. Through interviews, the inspectors found that the GVls of
Ol-AD-016 were interrupted on a regular basis by interfering activities and were
routinely not completed to the level that the operators interviewed felt that they
were meeting the requirements of the procedure,
The interview process was chosen by the inspectors for this determination because:
(1) there is no available objective evidence on which to judge whether these general
and routine requirements were being completed,
(2) the inspectors verified that field
audits by PPRL similarly concluded that there were weaknesses
in the NPO round
activities and, (3) it was anticipated that any NRC accompaniments
of NPO rounds
would not be interrupted by the type of activities described by the NPOs.
The inspectors verified through their interviews with NPOs, PCOs, Unit Supervisors
(USs), and Shift Supervisors
(SS) that portions of the GVls required by Ol-AD-016
sections 4.2 through 4.5 were delayed, amended or missed during periods of high
activity. The inspectors verified that neither Operations management
nor the NPOs
had documented the failure to implement OP-AD-016 as written in a condition
report (CR). This issue was discussed with SSES site management
on October 10,
1997 and with Operations department management
on October 16, 1997.
TS 6.8.1, Procedures,
requires procedures including Ol-AD-016 to be established,
implemented and maintained.
The failure to ensure that Operations department
procedure Ol-AD-016 was implemented as established
is considered
a violation
(VIO 387,388/97-07-02).
On October 17, 1997, the inspectors met with SSES site
management
and were presented with an action plan that included procedure
changes
and training topic additions that were intended to eliminate the procedural
compliance issue and clarify NPO performance expectations.
SSES management
stated that they considered certain parts of Ol-AD-016 to be general guidelines
which should be considered
in relationship to the NPO's experience
and training,
even though the procedure was written in a form that would require complete
implementation.
For example, step
1 of the General Rounds Expectations
attachment to Ol-AD-016 states that
~ .. All rotating equipment such as pumps,
motors shall be inspected each shift .. ~ Inspections of protective covers on MCC's
and load centers shall be performed .. ~ it is required to inspect all operator
accessible
areas of the plant ... The licensee changed the Rounds Expectations
attachment to read, for example, "When checking rotating equipment such as
pumps, motors, etc., consider the following.. ~ ", through procedure change PCAF 1-
97-0590 series.
This change clarifies that the requirements
are considered
guidelines, and provides the flexibilityfor more or less effort in given areas based on
other more significant shift activities.
The inspector concluded that the immediate
corrective actions were acceptable.
Conclusions
Interviews were conducted with non-licensed and licensed operators to assess
the
implementation of SSES Operations department procedure OI-AD-016, Operator
Rounds.
Based on these interviews, the inspectors determined that portions of
procedure sections-4.2 through 4.5 were routinely delayed, amended or missed
during periods of high activity. This issue was discussed with licensee management
on three occasions.
The licensee made changes to the procedure to ensure that the
procedure was clear and allowed shift supervision the flexibilityto delay or amend
the requirements for general equipment inspections in the subject procedure steps.
The licensee's immediate corrective actions were adequate
and were completed
prior to the end of the inspection period.
The failure to follow procedure OI-AD-01.6
as written during previous operator rounds was a violation of TS 6.8.1.
Operator Knowledge and Performance
0 erator Res
onse to 0 eratin
Occurrences
Ins ection Sco
e 71707
Control room operators were observed during performance of their on-shift
responsibilities throughout the inspection period.
For alarm conditions, the
inspectors verified that appropriate alarm response
procedures were implemented
and that the required actions were completed.
Observations
and Findin s
For the following alarmed conditions, the inspectors observed/reviewed
and verified
that appropriate alarm response
procedures were implemented.
AR 015-G6, Seismic Trigger
AR 214-01, HPCI Pump Suction Hi
AR-029-01, EDG Room Temperature
AR-051-01, Loose Parts Monitor
ON-200-05, Excess Drywell Leakage
C.
AR-016-H5, System Particulate Iodine Nobel Gas
AR-016-01, River Water Makeup
AR-009-01, Loss of River Water Makeup
h
Conclusions
The PCOs responded
well to alarmed conditions in the control room, in those cases
requiring actions.
PCOs were able to describe the reasons for their actions and
discuss the impact of their actions on the plant.
Each of the observed actions were
conservative and in accordance with established
plant procedures.
07
Quality Assurance in Operations
07.1
Corrective Action Team
CAT Su
ort of Plant 0 erations
a.
Ins ection Sco
e 71707
During the week of August 25, 1997, several issues were followed through the
Condition Report (CR) process and the functioning of the CAT'in support of plant
operations.
b.
Observations
and Findin s
The resolution of several issues was inspected.
These issues includqd loose pole
pieces on 4 kV electrical breakers and level indication maintenance
on the standby
liquid control system.
In each case the actions of the CAT team were direct, safety
oriented, and conservative.
However, during one specific observed CAT meeting,
the CAT was not aggressive
in ensuring that internal milestones for CR action item
closure were met, in that it granted completion date extensions with little
dlscusslon.
c.
Conclusions
The resolution of several issues by the PP&L Corrective Action Team (CAT) was
direct, safety oriented, and conservative.
08
Miscellaneous Operations Issues
08,1
Review of Licensee Event Re orts
a 0
Ins ection Sco
e 90712
The inspectors reviewed Licensee Event Reports (LERs) submitted to the NRC to
verify that the details of the events were clearly reported, including the accuracy of
the event description, cause,
and corrective action.
The inspectors evaluated
whether further information was required from the licensee, whether generic
implications were involved, and whether the events warranted onsite follow-up.
.7
Observations
and Findin s
The following LERs were reviewed and closed during this inspection period:
Closed
LER 50-387 97-010
On March 25, 1997, with Unit
1 in Condition 1, at 100% power, the. licensee
discovered, during a review of a hydrostatic pressure test procedure for Unit 2, that
during the Unit
1 hydrostatic pressure test performed in October 1996, the reactor
vessel low-level (Level 3) instruments had been isolated without entering the
Limiting Condition for Operation (LCO) for TS 3.3.2.
In addition, it was determined
that the time limits for the TS action statement
had been exceeded.
The root cause of this problem was determined by the licensee to be the use of a
draft TS amendment to prepare procedure revisions.
A list of approximately 380
procedures
requiring revision was generated
from the draft amendment.
The list
was not validated against the final approved amendment.
Exceeding the action
statement time limits of TS 3.3.2 was identified by PPRL as a condition prohibited
by TS and was reported per 10 CFR 50.73(a)(2)(l)(B).
The inspectors verified portions of the licensee's corrective actions which included
the revision of surveillance and test procedures,
the verification of the submitted TS
amendment data and the presentation of training topic reviews of the event to SSES
and corporate engineering personnel.
The inspectors determined that the errors
were related to personnel performance and that the existing PPSL administrative
procedure was adequate,
if implemented.
The associated
equipment for the isolated
instruments could have been manually actuated, if required.
This licensee identified and corrected violation is being treated as a non-cited
violation (NCV) consistent with Section VII.B.1 of the NRC Enforcement Policy.
(NCV 387/97-07-03) This NCV is closed.
Closed
LER 50-387 97-016
On July 3, 1997, with both Unit 1 and Unit 2 in Condition 1, at 100% power,
PPKL determined that the monthly surveillance to inspect fire hose stations had not
been completed within the TS 4.7.6.5.a required frequency.
The licensee further
determined that the frequency for performing this surveillance was exceeded
seven
times since January 1995.
In addition, the licensee determined that an associated
TS surveillance requirement of fire hydrants had exceeded
its frequency on one
occasion since January 1995.
These instances
are violations of TS in that they constitute conditions prohibited by
TS and are reportable per 10 CFR 50.73(a)(2)(i)(B). The licensee determined that
the cause of the events was a flawed scheduling tool used to track surveillances
against
a fixed date rather than the last performance date of the surveillance.
The
inspectors verified portions of the licensee's corrective actions which included
revising the method of tracking and scheduling performed surveillances and training
0
the appropriate plant personnel.
The inspectors further verified for a sample of
components that there was no pattern of surveillance failures of fire hose stations
or fire hydrants.
This licensee-identified and corrected violation is being treated as a
non-cited violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.
(NCV 50-387,388/97-07-04)
This NCV is closed.
Closed
LER 50-387 97-01
On July 2, 1997, with both Unit
1 and Unit 2 in Condition 1, at 100% power, the
licensee determined that it was not complying with TS Table 3.3.7.10-1, action
101
~ The TS require a gross radioactivity analysis on liquid effluent grab samples
when the associated
effluent monitoring instrumentation
is not operable.
The
licensee was performing a gamma isotopic analysis in such instances,
which does
not measure gross radioactivity to a sensitivity of 1x10'icrocurie/ml.
This is a
violation of TSs and was reportable per 10 CFR 50.73(a)(2)(l)(B). The cause of the
event was determined to be human performance.
In addressing the violation of TSs
the licensee stated
in its LER that "it was not recognized that a change to the TSs
was required since it was viewed that the isotopic analysis was an improved
method of analysis.
There were no safety consequences
or compromises to public
health and safety as a result of this event as the isotopic analysis is a better
analysis in determining radioactivity in effluents."
e
The inspectors verified portions of the licensee's corrective actions specific to this
TS which included, implementing the requirement to perform the gross radioactivity
analysis and proposing a revision to the TS to incorporate the second testing
methodology.
This licensee identified and corrected violation is being treated as a
non-cited violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.
(NCV 50-387/97-07-05) This NCV is closed.
C.
Conclusions
The events reported by PPRL in the LERs reviewed during this period were
appropriately reported, and provided an accurate description of the causes
and
corrective actions.
Based on a sample review of the licensee's corrective actions,
the inspectors determined that PP&L was implementing adequate corrective actions.
08.2
Review of NRC 0 en Items
Ins ection Sco
e 92901
The inspectors reviewed licensee corrective actions submitted to the NRC in
response to notices of violation.
In addition, licensee corrective actions for those
items that required follow-up were reviewed.
b.
Observations
and Findin
s
The following violations (VIOs) were reviewed during this inspection period:
Closed
VIO 50-388 97-03-01: Two examples of an Inadequate
Procedure
Two instances of inadequate safety related procedures
were identified,
One
procedure addressed
the movement of fuel assemblies
and other components within
the spent fuel pool. The second procedure addressed
an alarm response for an
indication of high radiation in the stack monitoring system.
The licensee responded
to this violation in PP&L letter PLA 4644 (Byram/NRC'Document Control Desk,
dated August 6, 1997). The licensee's corrective actions included procedure
changes, training, and the issuance of communications to involved SSES personnel
~
The inspectors verified portions of the licensee's corrective actions and determined
that the licensee's
response
was adequate.
This violation is closed.
U date
VIO 50-388 97-03-02:Core Spray System Surveillance Preconditioning
The licensee responded to this violation in PP&L letter PLA 4644 (Byram/NRC
Document Control Desk, dated August 6, 1997), and denied the validity of the
violation. The NRC responded to the licensee's
response
in NRC letter (Hehl/Byram,
dated August 26, 1997), upheld the violation and requested
additional information
and corrective action,
This violation remains open pending its final resolution.
Closed
VIO 50-388 97-03-03:Four Examples of a Failure to Perform a 10 CFR 50.59 Evaluation
In four instances,
PP&L failed to perform a 10 CFR 50.59 safety evaluation for
changes to plant facilities. The licensee responded to this violation in PP&L letter
PLA 4644 (Byram/NRC Document Control Desk, dated August 6, 1997). The
licensee's response was determined to be adequate
in that for each instance the
licensee addressed
the specific cause of the violation. The root causes identified by
the licensee were related to specific technical interpretations or personnel
performance issues.
Each of the specific corrective actions were reviewed by the
inspectors and determined to be adequate.
However, the licensee's response
and
corrective actions did not address whether previous or present programmatic
weaknesses
exist that may have contributed to the root cause of the violation. The
inspectors reviewed the violation and could not identify a common programmatic
problem or pattern.
Because the specific actions were adequate
and the PP&L
program description appears to be adequate, this violation is closed.
10
II. Maintenance
M1
Conduct of Maintenance
M1.1
Pre
lanned Maintenance Activit Review
a.
Ins ection Sco
e 62707
The inspectors observed/reviewed
selected preplanned maintenance
activities.
b.
Observations
and Findin s
The following WA activities were found to have been well performed.
The
maintenance activities were described and controlled with adequate,
but in some
cases general, procedures.
The maintenance
personnel performing the maintenance
were well trained, experienced,
and capable of explaining and discussing the
technical aspects of their assignea
functions.
The involvement of'the system
engineer in the planned maintenance activity was verified by the inspectors to be
appropriate for the specific instances.
PPRL continued to depend heavily on the
training and experience level of its work force, in addition to system
engineer/foreman
designated
maintenance
acceptance
testing, to ensure the quality
of performed maintenance.
This practice is in deference to providing more detailed
procedures
and increased management oversight.
This approach appeared to be
affective in the specific instances identified below.
WA S44545
High Pressure
Coolant Injection Cable Installation
WA P72390
"A" Residual Heat Removal Heat Exchanger Outage
WA S73559
"B" Recirculation Pump Motor Temperature Switch
WA H70004 "B" Emergency Diesel Generator 24-hour Run
WA S72470
Vent Plug Removal
WA V60717 Instrument Air/Service Air
WA V71705 Instrument Air/Service Air
W'A S73108
Containment Radiation Monitor Pump Replacement
WA S64976
Refueling Water Storage Tank Level Probe
WA H60536
Emergency Diesel Generator Turbocharger Coast down Time
WA P71161
Spent Fuel Pool temperature
WA S73786. Reactor Core Isolation Cooling
WA C73437
4 kV Switchgear
As part of the review of WA P72390, permits 1-97-1155, 1-97-1149, and 1-97-
1158 were also reviewed.
The permits were discussed with the operators and
reviewed against design drawings and control room indications to determine if the
permits adequately protected personnel from injury and safety related equipment
from damage.
These permits were determined to be adequate.
C.
11
Conclusions
The work authorization (WA) activities addressed
during this inspection period were
in general well performed.
The WAs described and controlled maintenance
activities with adequate,
but in some cases general, procedures.
The maintenance
activities were implemented by well trained and experienced
maintenance
technicians,
and resulted in equipment being returned to service in good condition.
M1.2
Pre
lanned Surveillance Activit Review
a.
- Ins ection Sco
e 62707
The inspectors observed/reviewed
selected preplanned surveillance activities to
ensure that the operability, availability and capability of safety related equipmer'.t
was maintained.
A special test of the instrument air system was also observed.
b.
Observations
and Findin s
SSES surveillance activities were found to be well performed.
The activities were
described and controlled in detail by SSES procedures.
The maintenance
and/or
Operations personnel performing the surveillances were well trained, experienced
and capable of explaining and discussing the technical aspects of their assigned
functions.
The involvement of the system engineer in the planned surveillance
activities and their performance briefings ("tailboard") were verified by the
inspectors to be appropriate for the specific instance.
The inspectors
observed/reviewed
the following preplanned surveillance activities.
SM-059-001
SO-1 59-002
TP-1 1 8-01 6
SO-252-002
SO-024-001
SO-1 53-004
18 Month Vacuum Relief Valve Set Pressure Test,
September
17, 1997
Stroke Test of Containment Vacuum Breakers,
September 3, 1997
Test of Instrument Air Cross-tie Valve PCV 12560,
September 3, 1997
HPCI Quarterly Surveillance, September
5, 1997
"A" Diesel Generator Monthly Surveillance, September 9, 1997
Standby Liquid Control Quarterly Surveillance,
September 9, 1997
C.
Conclusions
SSES surveillance activities, observed during this inspection period, were found to
be in general, well performed, described and controlled by detailed SSES
procedures,
and performed by well trained, experienced
and capable
technicians/operators.
~
M1.3
12
Maintenance Technician Task Certification
Ins ection Sco
e 62707
The inspectors reviewed the maintenance
department task certification matrix and
interviewed PPSL personnel that recently evaluated the implementation of the
maintenance task certification process.
b.
Observations
and Findin s
The inspectors reviewed a number of sources to determine if task certification was
being appropriately applied in safety related maintenance
activities.
Included in this
review was a PPSL Nuclear Assessment
Services (NAS) comparison of a large
number of WAs. The NAS comparison evaluated the task certifications of persons
doing the WA activities and found few discrepanciesThese
results agreed with the
findings of NRC Inspection Report 50-387,388/97-80,which found maintenance
department workers to be appropriately trained and task certified.
WA 55339 was reviewed.
This WA addressed
maintenance
performed on a non-
safety related positive displacement radiological waste pump (OP304B).
In addition,
the inspectors interviewed a PPKL representative
who had recently evaluated the
maintenance work performed on the pump.
The inspectors found that a first crew
of workers performed work outside of the tasks identified on the original WA, This
error resulted in the need for repeated work by a second crew, under supplemental
WA instructions, and delayed the return to service of the pump.
The inspectors
reviewed the certifications necessary for the maintenance tasks performed and
found that the personnel met SSES maintenance
program requirements.
Because
the maintenance
errors occurred on non-safety related equipment, and did not result
in a challenge to safety related equipment, no violation of NRC requirements was
identified.
On March 14, 1997, a crane. operator tipped over a 14 ton crane in the SSES yard.
This issue was addressed
in NRC inspection report 50-387,388/97-02.
The cover
letter for the inspection report requested the licensee to discuss the events in
writing. The licensee responded to the cover letter request in PPSL letter PLA 4632
(Jones/NRC document desk, dated June 27, 1997).
PPRL described its corrective
actions for the event in its response.
NRC Inspection Report 50-387,388/97-02,
section M2.1 stated that "a number of weaknesses
were identified by the licensee
and the inspectors including operator training and supervisory oversight" and that
the "event was similar to an inspector identified issue with the placement of a self-
propelled crane on a railroad rail near an excavation in 1996". The report concluded
that no violations of NRC requirements were identified.
The inspectors reviewed the licensee's corrective actions, associated
CRs, the PP5L
response to the NRC request for information, a PPRL audit of the event, an ERT
report which addressed
root causes for the event and PPSL Nuclear department
programmatic improvements in response to the event.
In addition to the prior
weaknesses
in the training of the crane operator and his supervision, this review
13
identified weaknesses
in the Nuclear department training and qualification process
for crane operators, which the licensee
is addressing.
No violations of NRC
requirements were identified; no programmatic links were identified (regarding task
certification of workers) between the weaknesses
associated with WA 55339 and
the March 14, 1997, crane event; and the licensee's
initial corrective actions for the
identified weaknesses
in both cases were adequate.
Some long term corrective
actions have yet to be completed.
No violations of NRC requirements were
identified in either case.
c.
Conclusions
The inspectors concluded that the maintenance task certification matrix and its
implementation were adequate to control the assignment of workers to safety
related maintenance activities.
No violation of NRC requirements were identified.
M2
Maintenance and IVlaterial Condition of Facilities and Equipment
M2,1
Tri
of the "C" Emer enc
Diesel Generator
Durin
Surveillance Testin
a.
Ins ection Sco
e 62707
The trip of the "C" EDG following the performance of a TS surveillance was
inspected/reviewed
during the course of normal surveillance observation.
b.
Observations
and Findin s
The inspectors observed portions of the surveillance and determined that the
operating portions of the surveillance were well controlled and implemented.
The
testing scheme was well briefed with the participating technicians, closely followed
and implemented by control room operators and adequately covered by PPS,L
procedures.
On August 18, 1997, following the completion of a 24-hour EDG run and load
rejection test, the EDG was allowed to run unloaded for 5 minutes and then the
stop
push-button was depressed
in accordance with procedure SO-024-001,
Monthly Diesel Surveillance.
Within forty five seconds of depressing the stop push-
button, the EDG tripped on indicated high jacket water temperature.
Other
indications of jacket water temperature showed that it was within normal operating
limits. When the EDG stop push-button
is pushed,
a 5 minute cool down of the
EDG is expected but, this did not occur.
The licensee initiated CR 97-2682 and WA S72651 to account for the failed
indication of jacket water temperature.
The CR contained
an operability
determination (OD) which stated that the temperature circuit and protective
functions are bypassed
in the emergency operation mode.
The OD also stated that
=the cause of the EDG trip was known, and that it had previously occurred as
documented
in CR.96-0184.
14
The inspectors determined that the corrective actions associated
with the two CRs,
and the interrupted cool down of the "C" EDG were adequate.
The licensee
determined that the interrupted cool down did not affect the operability of the EDG.
Conclusions
The licensee's corrective actions in response to an interrupted cool down of the "C"
EDG were adequate
and the interrupted cool down did not affect the operability of
the EDG.
Unit
1 "S" Safet
Relief Valve
SRV Acoustic Position Indicator Acoustic Monitor
Failure
Ins ection Sco
e 72707
On September
10, 1997, with Unit
1 in Condition 1, at 100% power, a control
room an'nunciator alarmed indicating that a Division 2 SRV had opened.
Operators
evaluated other plant parameters
and confirmed that the "S" SRV had not opened
although its acoustic monitor status lights were illuminated.
The inspectors
reviewed the licensee's actions in response to the acoustic monitor failure.
Observations
and Findin s
An investigation and surveillance were performed by instrumentation and control
technicians to evaluate the acoustic monitor failure.
In parallel with the
investigation, the licensee began preparations for requesting enforcement discretion
from the TSs that require an operable SRV acoustic monitor for the "S" SRV. After
reaching the conclusion that the acoustic monitor failure was inside containment,
PP&L requested
enforcement discretion, by letter dated September
11, 1997 (PLA-
4669).
PPRL requested
enforcement discretion to allow continued operation of the
Unit with the acoustic monitor inoperable, until an outage of sufficient duration
would allow drywell access,
but no later than the Unit
1 tenth refueling outage.
A conference call was held between the NRC and PPRL on the afternoon on
September
12, 1997. After discussion of the technical issues, prior equipment
failures, and alternate means of detecting an open SRV, enforcement discretion was
granted by Mr. John Stolz, Director, Project Directorate 1-2, Office of Nuclear
Reactor Regulation,
A supplemental letter (PLA 4670) documenting commitments
by PPSL during the conference
call was issued to the NRC later the same day.
The
NRC issued the written Notice of Enforcement Discretion (NOED) by letter dated
September
17, 1997.
PPSL submitted an emergency amendment request to the
NRC on September
15, 1997, to have the TSs changed to reflect the enforcement
discretion.
The TS amendment was issued by the NRC on September 23, 1997.
This issue will be evaluated for closure in conjunction with the routine NRC review
of Licensee Event Report 50-387/97-020-00,Operation
Prohibited By Technical
Specification - Loss of MSRV Acoustic Monitor.
15
c ~
Conclusions
PP&L requested enforcement discretion for TS requirements concerning
a failed
acoustic position indicator for the "S" Safety Relief Valve.
PPS.L requested the
discretion to avoid an undesirable transient as a result of forcing compliance with a
license condition.
The NRC approved PPSL's request after determining the action
involved minimal or no safety impact and had no adverse radiological impact on
public health and safety.
M3
IVlaintenance Procedures
and Documentation
M3.1
Release of Unit
1 Standb
Li uid Control
SBLC Accumulator Work
Ins ection Sco
e 62707
On September 9, 1997, the inspector observed work on the "A" SBLC accumulator
when no TS limiting condition for operation had been entered.
The inspectors
reviewed the control of work and PPS.L's basis for determining that the accumulator
work would not affect the operability of the "A" SBLC pump.
b:
Observations
and Findin
s
The "B" SBLC pump was taken out of service for planned maintenance at 5:00 a.m.
on September 9, 1997.
The "B" SBLC pump motor's power supply was de-
terminated and consequently, the Unit Supervisor documented entry into TS 3.1.5
Action a.1. With one SBLC pump inoperable, Action a.1 requires the licensee to
restore the inoperable pump within 7 days or be in at least Hot Shutdown withing
the next 12-hours.
TS 3.1.5 Action a.2. requires that with the SBLC system
otherwise inoperable, the system must be restored within 8-hours or the unit must
be in the Hot Shutdown condition within the next 12-hours.
On the morning of September 9, 1997, the inspectors found that maintenance
personnel had depressurized
the "A" SBLC accumulator to repair the accumulator's
charging valve under WA H70595 while work on the "B" SBLC pump was still in
progress.
The maintenance
personnel were performing actions to ensure the "A"
SBLC pump's accumulator was charged according to MT-053-003, SBLC
Accumulator Maintenance.
This activity is routinely completed prior to the SBLC
quarterly surveillance as directed by step 5.7 of SO-153-004, Quarterly SBLC Flow
Verification, Revision 21. The inspectors noted that SO-153-004did not contain
precautions regarding performance of this step relative to operability impact.
The
maintenance activity is performed in support of SO-153-004under
a blanket WA
which is used to track workers time. After further review, the inspectors found that
neither maintenance
procedure MT-053-003, Revision 5, nor the WA contained
precautions or notes regarding the impact on SBLC operability.
The inspectors discussed the release of this work with the responsible Unit
Supervisor (US). The US's activities and the maintenance
personnel's actions were
supported by their respective procedures.
According to the US, his decision to
16
allow work on the '='A" SBLC accumulator was influenced, in part, by the fact that
this activity had been done the same way for a very long time and was not
previously considered to have an operability impact.
The inspectors discussed, with the cognizant NSE system engineer, the potential
impact of having no accumulator.
Two possible effects were discussed,
the
potential to liftthe pump's discharge line relief valve, diverting injection flow and
the potential to invalidate assumptions
in the SBLC piping analysis.
Based on review of the procedural controls for the accumulator work and
discussions with cognizant NSE personnel, the inspectors concluded that PPSL did
not have
a pre-existing analysis to support depressurizing
an accumulator and still
consider the associated
SBLC pump operable.
TS 6.8.1 requires written procedures
be established,
implemented, and maintained covering the procedures recommended
in Appendix A of Regulatory Guide (RG) 1.33, Revision 2, February 1978.
Item 9,a.
of Appendix A to RG 1.33, requires procedures for maintenance that can affect the
performance of safety related equipment.
PPKL failed to provide an adequate-
procedure for, the control of the accumulator maintenance,
since the impact of the
activity was not clearly understood.
This failure is considered
a violation of TS 6.8.1.
(VIO 50-387/97-07-06)
The inspectors discussed the potential TS compliance issue with a NAS
representative
who was observing the work as part of a surveillance for "Potential
Preconditioning of Equipment Prior to Testing".
The NAS surveillance was
performed as an initiative in response to recent SSES and industry events (reference
VIO 50-387/97-03-02).
The NAS representative
took appropriate actions to follow-
up the TS compliance issue and initiated CR 97-2958.
The NAS representative
also
initiated CR 97-2973 to document his observation. that charging the SBLC
as a prerequisite to the surveillance test, may precondition the
system.
After the issue was brought to Operations by NAS, an initial operability
determination was prepared by the Shift Technical Advisor (STA) who discussed the
issue with the system engineer.
The operability determination states:
The accumulators were originally designed to provide over-
pressurization protection along with several other design
improvements.
The existing system configuration has a relief
valve at the discharge of each pump which would provide this
protection.
~ . There is industry experience that also suggests
that the accumulators may not be needed
and based on the
system configuration have been subsequently
eliminated.
The inspectors considered the initial operability determination technically incorrect in
its description of the accumulator function and weak in that it did not address the
known technical issues with the potential to affect operability.
The fact that other
plants have removed accumulators did not establish the operability of the system at
SSES without plant specific analysis.
However, the inspectors considered the
0'
17
safety impact of this event low since the accumulator was restored to its original
configuration in less than one hour (before the STA's operability determination).
fven if PPSL's CR investigation and root cause determine TS 3.5.1 Action a.2.
should have been entered, the actual duration of the "A" SBLC pump work was
significantly less time than allowed by the TS.
The routine charging of SBLC accumulators before required surveillance testing, and
the training provided to STAs on operability determinations, will both be addressed
during the closeout of the violation.
C.
Conclusions
PPSL allowed maintenance work to proceed on the "A" Standby Liquid Control
(SBLC) pump nitrogen accumulator without evaluating whether the activity would
affect operability. After the question of operability impact was raised by the NRC,
an initial operability determination by the Shift Technical Advisor was weak because
it did not address known technical issues with the potential to affect operability.
The failure to provide adequate
procedures for control of maintenance
on safety
related equipment is a violation of TSs.
M7
Quality Assurance
in Maintenance
M7.1
Unit
1 RHR Pum
"A" Recirculation Check Valve Ins ection
~
~
a.
Ins ection Sco
e 62707
On August 19, 1997, the inspectors observed
a portion of the preventive
maintenance activity used to meet inservice test program (IST) requirements for the
residual heat removal (RHR) check valve 151-F046A. This activity was performed
as part of an on-line maintenance work window for RHR Division I equipment under
WA P71715.
b.
Observations
and Findin s
The RHR minimum flow check valve is a 4" bonnet hung check valve mounted in a
vertical pipe.
In 1994, a similar 3" check valve failed to prevent reverse flow in the
core spray system.
During the 1994 occurrence, the dimensional tolerances of the
core spray check valve allowed less than full coverage of the valve seat by the disk.
The result was minor reverse flow through the valve. At SSES, sixteen bonnet
hung check valves are used in core spray and RHR systems.
On August 19, the inspectors questioned how the corrective actions from the 1994
problem had been incorporated into preventive maintenance WA P71715.
The
maintenance
foreman stated that the Valve Team requested
certain measurements
and that they had provided a drawing to illustrate the tolerances of interest.
18
The inspectors determined that the informal tolerance checks, uncontrolled
document and acceptance
criteria being used to assess
the condition of the check
valve were corrective actions for a previous condition adverse to quality. This
concern was discussed with the maintenance
foreman and a NAS - Surveillance
Services representative.
On August 25, 1997, the Valve Team supervisor initiated CR 97-2775 to document
that a corrective action for CR 96-1902 was not appropriately closed.
This 1996
CR documented that a Unit 2 "A" Core Spray (CS) minimum flow check valve
inspection found another example of the 1994 tolerance problem.
Although CR 96-
1902 required all core spray and RHR minimum flow check valves be inspected, the
administrative process to track this action was not initiated.
On August 26, 1997, a NAS - Surveillance Services representative
initiated
CR 97-2786.
This CR documents that the corrective actions for a 1994 Significant
Operating Occurrence Report and a 1994 Non-Coriformance Report did not address
the inspection of similar check valves.
CR 97-2786 also identifies the corrective
action tracking problem discussed
in CR 97-2775, but adds the perspective that
preventive maintenance WA's performed since 1994 have informally checked the
subject tolerances.
The inspectors concluded that PPRL failed to take adequate
corrective actions in
1994 and in 1996 for the check valve tolerance deficiencies.
The inspectors
considered the safety significance of minor CS or RHR minimum flow, check valve
back-leakage
under design basis conditions to be minimal ~ However, this problem
could result in damage of safety related equipment during routine surveillance
testing.
The previous corrective action problems are in the licensee's corrective
action process,
are being evaluated,
and had no impact on the safe operation of the
plant.
This failure constitutes
a violation of minor significance and is being treated
as a non-cited violation, consistent with Section IV of the NRC Enforcement Policy.
(NCV 50-387,388/97-07-07)
Conclusions
Corrective actions for a safety related check valve deficiency identified in 1994 did
not address the generic issue.
In 1996 the same condition was identified on a
different valve and, in this case, the planned actions to prevent recurrence were
appropriate.
However, the administrative process to implement and track these
actions was not initiated. These two corrective action problems are considered
a
violation of minor significance because there was no impact on safety.
Condition Re ort CR Su
ort for Maintenance Activities
Ins ection Sco
e 62707
Inspection activities were conducted to determine if the CR process was being
made use of in the course of Maintenance department activities, including the
willingness of Maintenance department personnel to make use of the CR process.
,19
b.
Observations
and Findin s
The inspectors reviewed a PPSL compilation of CRs that resulted from Maintenance
department workers.
The sources of the.CRs spanned
a representative
cross
section of the Maintenance department and the technical issues were varied.
A
PPSL survey that represented
interviews with a large number of SSES maintenance
workers was reviewed by the inspectors.
The conclusions from the survey were
that maintenance workers were aware of the CR process
and were willingto use
the process to correct problems.
During the course of normal inspection activities
the inspectors discussed
the CR process with SSES maintenance workers.
The
results of the NRC conversations with the SSES maintenance workers were similar
to those conclusions in the PPRL survey.
Although some maintenance
personnel
expressed
reservations
regarding the effectiveness of the CR process, the workers
interviewed were willing to submit CRs when necessary.
No violations of NRC
requirements were identified.
C.
Conclusions
A PPRL compilation of Maintenance-department
generated
condition reports (CR)
was reviewed.
The CRs were generated
by a representative
cross section of the
Maintenance department and the technical issues were varied.
The conclusions of a
PPRL survey were found to be consistent with NRC interviews in that maintenance
workers were found to be aware of the CR process
and were willingto use the
process to correct problems,
E2
Engineering Support of Facilities and Equipment
E2.1
Reactor Core Isolation Coolin
RCIC Drain Pot Level Switch
Ins ection Sco
e 37551
P
The condition of the Unit 1 RCIC drain pot level switch was reviewed/inspected
to
evaluate the licensee's control over the current degradation of the RCIC steam line
drain piping and to ensure that the degradations
did not result in another plant
transient (see
IR 50-387, 388/96-11).
b.
Observations
and Findin
s
The control, trending and tracking of the RCIC drain line pipe degradation was
partially implemented under WA S79877. The licensee's
engineering diagnostic
actions were determined to exceed those actions recommended
by EPRI and to be
comprehensive.
The 1996 RCIC system piping degradation was evaluated to be the
result of flow impingement and general erosion.
From the standpoint of the erosion
control program, engineering corrective action was determined to be outstanding.
,20
From a second perspective, the drain pot was bypassed
and allowed the drain line
to degrade,
and a continuous alarmed condition existed in the control room for a
period of approximately ten months following the unscheduled
plant shutdown that
resulted from the RCIC drain line failure (see IR 387,388/96-11).
A modification
that replaced the drain pot level switch with a different type switch was completed
during this inspection period under Design Change Package
(DCP) 97-9060.
This
modification appeared
to be effective in preventing
a high level condition in the
RCIC drain pot and removed the alarmed condition in the control room.
The
corrective actions to resolve the RCIC steam line drain pot problems were not
aggressive;
resulted in a system important to safety being operated outside of its
normal alignment for greater than two years; did not prevent an unscheduled
plant
shutdown; and displayed an alarmed condition in the control room for an extended
period of time.
Conclusions
The erosion control program portion of engineering corrective actions for an
indicated high level in a reactor core isolation cooling drain pot was determined to
be outstanding.
The engineering corrective actions for problems with the Unit
1
RCIC drain pot level switch were not timely. This allowed continuous degradation
of the drain line and a continuous alarmed condition for over ten months after it
caused
a forced shutdown.
A modification to replace the drain pot level switch was
completed and has been effective in restoring the normal operation of the RCIC
system.
E4
Engineering Staff Knowledge and Performance
E4.1
Control Structure Chiller Automatic Start Ca abilit
a e
Ins ection Sco
e 37551
On July 15, 1997, the inspectors reviewed open temporary modifications for Unit 1
controlled under the Bypass Program described
in NDAP-QA-484. Bypass 0-97-005
for the "B" Control Structure (CS) chiller was selected for additional review based
on its apparent safety significance and questions regarding the ability of the standby
"A" CS chiller to start automatically.
Observations
and Findin s
The CS chillers provide the safety related cooling supply to electrical equipment in
the CS and the 4 kV emergency switchgear for Unit 1. Section 9.2.12 of the SSES
FSAR states that a start of the standby control structure chilled water train will be
automatic on failure of the operating train.
FSAR Table 9.2-15 shows
a failure
modes and effects analysis for the CS chilled water system.
For the assumed
failure of a chiller, the chilled water loop circulating pump trips and the standby
chiller train starts automatically.
21
Bypass 0-97-005 states that removal of an existing jumper on the safety indication
panel (SIP) for the "8" CS chiller will ensure that a trip of the "B" chiller remains
sealed in. This design will assure that the "A" CS chiller, when in "standby," will
automatically start.
The Bypass states that this configuration meets the design
intent of the chiller logic.
During a review of open Bypasses
on July 15, 1997, the inspectors questioned
whether the plant had been operated outside its design basis in the past when the
"B" CS chiller was in service.
This issue was subsequently discussed with Nuclear
Licensing and Nuclear System Engineering personnel.
The problem with the "B" CS chiller was first identified on February 27, 1997.
Although PP&L captured the wiring error in CR 97-0434 and corrected the condition
as of March 1, 1997, PP&L failed to recognize that the plant had previously been
operated outside the design basis.
After discussions with the inspector, the
licensee issued CR 97-2641 on August 13, 1997, to document this discovery.
In
the reportability evaluation for CR 97-2641 PP&L determined this condition was
reportable under 10 CFR 50.73.
LER 50-387/97-019-00was
submitted to the NRC on September
11, 1997. The
LER states that the "A" CS chiller would not have automatically started as designed
if the "B" CS chiller tripped on low oil pressure,
but would have started on any
other trip of the "8" CS chiller. This condition was determined to have existed
since initial startup of the. plant and was the result of a change
in the chiller logic
during pre-operational testing.
The inspectors determined that this condition should
have been reported by PP&L in March 1997.
PP&L concluded that the root cause
for the late NRC notification was a less than adequate reportability determination by
the Operating Experience Services organization.
As corrective action, PP&L
completed reportability training for the OES organization.
This training willcontinue
as refresher training and as part of the initial training for new OES personnel.
The inspectors reviewed the training outline and class attendance
roster for PP&L
course nomber AD064, Reportability Determination, the training referenced
in the
LER. The training outline referenced
NRC reportability guidance in NUREG 1022 and
described practical examples that require students to evaluate scenarios using the
applicable SSES procedure and the NRC guidance.
The inspectors considered the
training outline to be thorough.
Based on the training roster, the inspectors
concluded that the OES personnel involved in the LER issue, members of PP&L's
licensing staff, and other members of the OES staff had attended the training.
10 CFR 50.73(a)(2)(ii)(B) requires licensees to report any condition that was outside
the design basis of the plant.
In this case,
PP&L initiallyfailed to recognize the
previous condition as outside the design basis.
However, the technical problem
was limited to a very specific problem with a single chiller and was promptly
corrected by the licensee upon identification. After the problem with the
reportability evaluation was identified, PP&L appropriately submitted an LER
discussing the technical issue and the inadequate reportability determination.
developed and implemented corrective actions to address their root cause findings.
22
The instructor guide and attendance
records for the reportability evaluation training
were reviewed and verified by the inspector.
The failure to report oper'ation in a
condition that was outside the plant's design basis within 30 days of discovery is a
violation of 10 CFR 50.73.
However, this failure constitutes
a violation of minor
significance and is being treated as a non-cited violation, consistent with Section IV
of the NRC Enforcement Policy. (NCV 50-387/97-07-08)
C.
Conclusions
PP5L identified that the "A" CS chiller would not automatically start as designed
in
February 1997 and took immediate actions to correct the problem.
However, PPRL
initially failed to recognize this condition as outside the plant's design basis, as
described
in the Final Safety Analysis Report.
After identification by the NRC, PPSL
initiated a Condition Report, determined the condition was reportable, and submitted
a Licensee Event Report as required.
Corrective actions for both the technical
problem and the failure to recognize the condition outside the design basis were
implemented by PP&L.
In this case, the failure to report a condition outside the
design basis within 30 days of discovery is characterized
as a non-cited violation.
E4.2
Hi h Pressure
Coolant In'ection
HPCI 0 erabilit
Determination
a 0
Ins ection Sco
e 37551
On August 6, 1997, operators observed
an unusual sequence
of HPCI stop and
~ control valve movement during a weekly auxiliary oil pump preventive maintenance
(PM) activity. The inspectors reviewed the licensee's operability determination for
the apparent degradation of the HPCI system.
b.
Observations
and Findin s
The HPCI lube oil system has two pumps, a shaft driven pump that provides oil
when the turbine speed is greater than 1500 rpm, and a motor driven auxiliary oil
pump for when the turbine speed is less than 1500 rpm. When HPCI receives an
initiation signal, the auxiliary oil pump starts to provide the motive force for opening
of the HPCI stop and control valves.
PPRL performs a weekly PM activity that
starts the auxiliary oil pump causing the HPCI stop and'control valves to cycle as
they would for an automatic start.
On August 6, 1997, operators observed
an unusual sequence
of HPCI stop and
control valve movement during a weekly auxiliary oil pump PM activity. The
operators'bservation
was documented
in CR 97-2568 and an operability
determination was prepared by NSE. The NSE investigation of the event determined
that the HPCI turbine's overspeed trip assembly had unexpectedly actuated
following the auxiliary oil pump start.
This trip interrupted the opening cycle of the
turbine stop and control valves, causing them to close.
Approximately five seconds
after the trip, the overspeed
assembly automatically reset (as designed)
and the
valves began their open sequence
a second time.
23
The original operability determination for CR 97-2568 reasoned that computer
traces showed the HPCI valves would respond to an initiation but that it would take
HPCI approximately five seconds
longer to inject than normally expected.
PPS,L
considered
the system would still meet its 30-second
injection time design basis, even with this delay.
The HPCI injection valve receives an open signal from a limit switch on the turbine
stop valve.
The injection valve's control logic has a seal-in feature to ensure the
valve completes its intended open or close stroke before changing direction.
On
August 7, 1997, the inspectors questioned how the HPCI injection valve response
time would be affected by the interruption of the normal HPCI turbine valve
sequence.
PPKL's review, in response to the inspector's questions, identified the potential for
the HPCI injection valve to begin closing after completing its open travel in response
to a system initiation. Although it is designed to reopen, the delivery of full HPCI
injection flow could take up to 36 seconds.
Based on this discovery, PP5L declared
HPCI inoperable on August 7, 1997, and reported the loss of the single train safety
system to the NRC as required by 10 CFR 50.72.
CR 97-2596 was initiated to
document this discovery.
On August 15, 1997, NSE"revised the HPCI operability determination and concluded
that the system could perform its intended safety function with the subject
degradation.
PPSL's evaluation developed two approaches
to support their
conclusion that HPCI had been degraded but remained operable.
In the first
approach,
PPS.L used historical stroke time data to show that the overspeed trip and
reset would not cause the injection valve to close.
However, the margin credited in
this evaluation was 0.25 seconds.
Since this margin was not significant, PPS.L
developed
a second approach assumed the injection valve does go closed, but
credits the injection valve's ability to pass full HPCI flow before reaching the full
open position.
The inspectors reviewed the licensee's completed CR evaluation, HPCI start time
lines, and the engineering calculation for flow capability of the injection valve.
No
problems were identified with PPRL's reevaluation of HPCI operability. The
inspectors considered the second approach, which took credit for the flow
capability of the injection valve at less than full open, a stronger basis for
operability.
The inspector's review of this issue did not identify any violations of
NRC requirements.
Corrective maintenance
activities, with significant NSE and consultant involvement,
were effective in resolving the unexpected
overspeed trips on the start of the
auxiliary oil system.
Following completion of the maintenance
on August 15, 1997,
no unexpected trips of the overspeed tappet occurred and the licensee is continuing
to monitor the system performance closely.
,24
C.
Conclusions
The initial operability determination for the Unit 2 high pressure coolant injection
(HPCI) overspeed trip assembly problem was weak.
Nuclear System Engineering
personnel overlooked the potential impact on the HPCI injection valve and how this
impact could affect the response
time to rated flow. PPRL management
made a
conservative decision to declare
HPCI inoperable, pending further evaluation.
A
subsequent
revision of the operability determination provided a good basis for
operability.
Significant licensee attention was focused on resolution of the problem
and the overspeed trip assembly has performed acceptably since the corrective
maintenance.
Miscellaneous Engineering Issues
E8.1
Unit 2 Reactor Buildin Truck Ba
Hatch
a.
Ins ection Sco
e 71707 37551
The inspectors observed that a large floor hatch on elevation 749 of the Unit'2
reactor building was open and appeared to have been that way for many years.
This hatch separates
elevation 749 from the reactor building truck bay.
The
inspectors questioned the impact of the open door on the plant's design basis.
Observations
and Findin s
The NSE personnel reviewed the requirements for closure of plant hatches
in
response to the inspector's question.
Calculation EC-012-2419 lists 26 hatches
that are required to be closed and secured
based on the assumptions
used in the
design basis tornado analysis.
10 CFR 50, Appendix A, Criterion 2, requires
structures important to safety be designed to withstand the effects of natural
phenomena
such as tornadoes without loss of capability to perform their safety
functions.
To investigate this issue further NSE personnel performed a plant walk down to
verify the correct position and appropriate "tie-downs" for all 26 hatches listed in
the tornado analysis.
On June 11, 1997, PPSL initiated CR 97-1950 to document
that the Unit 2 truck bay hatch on elevation 749 of the reactor building was open
and that hatch "H2" located in the "C" EDG bay did not have "tie-downs" installed.
Immediate actions for this CR included the closure of the truck bay hatch and
installation of "tie-downs" on hatch "H2."
PPSL's actions to prevent recurrence for CR 97-1950 include a revision to
procedure NDAP-QA-0409, Door, Floor Plug and Hatch Control, to identify hatches
that must be closed and secured to meet the tornado analysis assumptions.
Also,
an analysis is being done to support opening of these hatches during all plant
operating conditions.
PP&L considers completion of this analysis necessary
before
opening the hatches listed in the tornado analysis and NDAP-QA-0409 provides an
administrative control to ensure this is done.
The analysis is targeted for
completion in January 1998.
25
The inspectors questioned whether PP&L's ongoing review of the current licensing
basis, as described
in a letter to the NRC dated February 13, 1997, would have
identified that the hatch position did not match the assumptions
in the tornado
analysis.
On October 17, 1997, the inspectors met with SSES and PP&L
engineering personnel to determine if the PP&L current licensing basis process
would have identified this issue.
Based on the information provided at this meeting,
the inspectors determined that licensee's
program to review their licensing and
design basis and update the UFSAR would not have identified this issue.
Therefore,
the enforcement discretion per Section VII.B.3 of the NRC enforcement policy could
not be applied.
PP&L's resolution plan for CR 97-1950 includes a re-analysis of the tornado design
basis scheduled for completion in January 1998.
Based on these results, PP&L will
decide whether an unreviewed safety question (USQ) existed.
The open Unit 2 truck bay hatch was not previously addressed
by an engineering
analysis.
No safety evaluation was performed in accordance with 10 CFR 50.59 to
determine if a USQ would result from the changing the, hatch configuration
previously assumed
in the tornado analysis.
The failure to perform the safety
evaluation required by 10 CFR 50.59 is considered
an apparent violation. PP&L's re-
analysis of the torna'do design basis and evaluation of the potential USQ will be
reviewed, in part, to determine the safety significance of this apparent violation.
This item is open, pending PP&L's reanalysis and is being tracked as an unresolved
item.
(URI 50-387,388/97-07-09)
c.
Conclusions
PP&L failed to perform a 10 CFR 50.59 safety evaluation prior to opening a plant
equipment'hatch
assumed to be closed by the tornado design basis analysis.
This
condition existed for an extended period before identification by the NRC. Plant
equipment hatches
have been verified to be in the condition assumed
by the
tornado analysis (shut) and are now being administratively controlled.
PP&L's
evaluation to determine whether an unreviewed safety question existed with the
hatch open is expected in January 1998 and will be reviewed to determine the
safety significance of this violation.
In the interim, this item is being tracked as an
unresolved item.
E8.2
Station Blackout Desi
n Basis
a.
Ins ection Sco
e 37551
A review of the SSES responses
to 10 CFR 50.63, Station Blackout (SBO) rule was
conducted to determine if SSES met the established
design requirements for SBO
coping duration and auxiliary power sources.
26
b.
Observations
and Findin s
The licensee installed an auxiliary diesel power source to increase the SSES SBO
coping duration of its 125 Vdc batteries from approximately 5-hours to in excess of
8-hours.
In order to ensure this coping duration extension, it is necessary to ensure
that the auxiliary diesel power source is maintained in an available condition.
The
licensee currently tests the auxiliary diesel power source once a year. for a short
duration.
However, the licensee does not perform the vendor recommended
equipment preventive maintenance/surveillance
schedule,
and does not maintain the
equipment within the quality requirements of 10 CFR 50 Appendix B.
The
inspectors reviewed portions of the following referenc'es to determine if the licensee
was required to meet an SBO coping requirement of greater than 4-hours.
PPSL References
1.
2.
3.
4.
5.
6.
7.
PPSL letter,
PPSL letter,
PPSL letter,
PP5L letter,
PPS.L letter,
PP&L letter,
PPS.L letter,
Keiser/NRC public document room,
Keiser/NRC public document room,
Keiser/NRC public document room,
Keiser/NRC public document room,
Keiser/NRC public document room,
Keiser/NRC public document room,
Keiser/NRC public document room,
NRC References
dated
dated
dated
dated
dated
dated
dated
April 17, 1989
April 17, 1990
February 27, 1991
August 1, 1991
March 13, 1992
April 14, 1992
May 13, 1992
1.. Safety Evaluation, dated January 14, 1992
2.
Supplemental Safety Evaluation, dated June 16, 1992
NRC reference
2 determined that it was only necessary
for the licensee to meet a 4-
hour coping duration.
This requirement can be met with the currently available 125
Vdc batteries.
Therefore, the inspectors determined that there was no current
regulatory requirement for the licensee to maintain the auxiliary power source.
C.
Conclusion
A review of the SSES responses
to 10 CFR 50.63, Station Blackout (SBO) rule was
conducted to determine if SSES met the established
design requirements.
The
licensee installed an auxiliary diesel power source to increase the SSES SBO coping
duration of its 125 Vdc batteries from approximately 5-hours to in excess of 8-
hours.
The NRC safety evaluation report concluded that SSES must meet a 4-hour
coping condition. Therefore, the inspectors concluded that there was no current
regulatory
requirement for the licensee to maintain the auxiliary power source.
E83
a.
27
Floatin
Service Platform on Safet
Related S ra
Pond
Ins ection Sco
e 37551
The inspectors observed that a large floating service platform was being stored on
safety related spray pond that is the ultimate heat sink for both SSES units.
The
spray pond services the emergency service water (ESW) and residual heat removal
service water (RHRSW) systems.
The inspectors questioned the impact of the
floating service platform on the performance of safety related equipment associated
with the spray pond.
b.
Observations
and Findin s
The NSE and licensing personnel were interviewed to determine if design
documentation existed for the platform, which was used as a special tool during
spray nozzle maintenance.
The licensee was not able to identify design
documehtation for the design, fabrication, or installation of the floating platform.
In
addition, the licensee was not able to identify documentation to show that a safety
evaluation was performed prior to the placement of the floating platform on the
No safety evaluation was performed in accordance with 10 CFR 50.59
to determine if a USQ would result from placing a floating platform on the spray
pond.
Subsequent
to the inspectors'uestions,
the licensee removed the platform
from the spray pond.
The failure to perform the safety evaluation, as required by
10 CFR 50.59, is a violation. (VIO 50-387,388/97-07-10)
On October 17, 1997, the inspectors met with SSES and PPSL engineering
personnel to determine if the PPRL current licensing basis process would have
identified this issue.
Based on the information provided at this meeting, the
inspectors determined that the licensee's
program to review their licensing and
design basis and update the UFSAR would not have identified this issue.
Therefore,
the enforcement discretion per Section VII.B.3 of the NRC enforcement policy could
not be applied and this item is being cited.
Analysis of the spray pond design basis
and evaluation of the potential USQ will be, reviewed with the response to this
violation.
C.
Conclusions
PP5L failed to perform a 10 CFR 50.59 safety evaluation prior to placing a floating
service platform on the spray pond that serves as the ultimate heat sink for both
SSES units. This condition existed for an extended period before identification by
the NRC. The spray pond was verified to be in the condition assumed
by the Final
Safety Analysis (the platform was removed).
PPSL has yet to perform an
evaluation to determine whether an unreviewed safety question existed with the
platform on the spray pond.
Analysis of the spray pond design basis and evaluation
of the potential USQ will be reviewed with the response to this violation.
28
IV. Plant Su
ort
F2
Status of Fire Protection Program
F2.1
Control Room CO, Fire Protection S stem
a.
Ins ection Sco
e 83750
The licensee's programmatic response to a potential fire in the control room was
reviewed.
b.
Observations
and Findin s
The SSES control room fire suppression
system was determined to be a manually
initiated system which actuates
on a delayed basis.
It uses CO, gas injected
beneath the control room electrical cabinets and the control room floor. This
system will not actuate automatically.
On a CO, system initiation, whether the
initiation is valid or not, the licensee has two off normal (ON) procedures
in place to
affect an evacuation of the control room and respond to a fire in the control room:
ON-013-001, Response to Fire and ON-100-009, Control Room Evacuation.
The immediate actions required by these procedures
are to declare there is a fire
and/or habitability problem in the control room, initiate a manual scram, evacuate
the control room, and then initiate a safe shutdown of the units from the remote
shutdown panel.
There is no SSES expectation that operators will remain in the
control room after a control room evacuation is determined to be necessary.
Therefore, self contained breathing apparatus
(SCBAs) are identified by SSES plant
procedures for use only by the fire brigade and are not required or intended for
operator use in the control room, as an alternative to abandoning the control room.
C.
Conclusions
The licensee's programmatic response to a potential fire in the control room was
reviewed and determined to rely on off normal procedures which require the manual
initiation of a CO, fire protection system and the immediate evacuation of the
control room. The controls established
by the licensee to ensure that control room
operators do not require the use of self contained breathing apparatus
(SCBA),
during a fire and/or habitability problem in the control room. These controls were
determined to be adequate.
R7
Radiological protection and Chemistry (RPC) Controls
R7.1
Health Ph sics Friskin
Problems and Corrective Actions
a.
Ins ection Sco
e 83750)
NRC Inspection Reports 50-387,388/96-04and
97-02 discussed
problems with
health physics (HP) frisking practices using hand held contamination monitors, and
,
29
the licensee's
response
to those frisking issues.
The latter inspection found that
appropriate frisking techniques were used during NRC observations,
and that
assistant
HP foreman were providing close oversight of contract HP technicians.
This inspection reviewed associated
HP performance as identified in PP&L condition
reports (CRs) to determine whether any continuing problems were evident in this
area.
b.
Observations
and Findin s
The inspectors reviewed a PP&L compilation of approximately 104 HP department
CRs and discussed the CRs with representatives
of the HP organization, the
Independent Safety Evaluation Services, and Nuclear Assessment
Services.
During
these discussions,
the inspectors questioned the licensee's review and disposition
of the CRs.
In specific, only three CRs from the Unit 2 eighth refueling outage
identified problems with either "frisking" or "contractors".
No trend was found by
the inspectors or PP&L among the three CRs, since each of the CRs dealt with
different technical aspects,
and each of the CRs appeared to have adequate
corrective:action implemented.
The inspectors verified that the licensee implemented corrective actions from a CR
(96-0106) that dealt with improvements to monitoring equipment, postings and
changes to policies that govern removal of potentially contaminated materials from
the Radiological Controlled Area.
The inspectors reviewed the licensee's evaluation of the compilation of HP CRs
discussed
above,
and an ISES review of the above
mentioned CRs and HP issues.
No programmatic trends were identified regarding
frisking practices with hand held monitors; and the licensee's initial corrective
actions for the specific identified weaknesses
in the three CRs inspected were
adequate,
C.
Conclusions
An evaluation of condition reports (CRs), from the Unit 2 eighth refueling outage,
concluded that there was no continuing trends regarding inadequate frisking
practices with hand held monitors.
The licensee's initial corrective actions for the
identified weaknesses
in the three CRs inspected were adequate.
X1
Exit Meeting Summary
The inspectors presented
the inspection results to members of licensee management
at the conclusion of the inspection on October 20, 1997. The licensee
acknowledged the findings presented.
0
P
,30
~Oened
ITEMS OPENED, CLOSED, AND DISCUSSED
50-387, 388/97-07-01
50-387, 388/97-07-02
50-387/97-07-06
50-387,388/97-07-09
50-387,388/97-07-1 0
Closed
IFI
Equipment Failure Root Cause Evaluations
Inadequate
Implementation of Operator Rounds
Inadequate
Procedures for SBLC Maintenance
Re-analysis of the Tornado Design Basis
Floating Platform on the Spray Pond 50.59
50-387/97-01 0
50-387,388/97;07-03
50-387/97-01 6
50-387,388/97-07-04
50-387/97-01
50-387/97-07-05
50-387,388/97-07-07
LER
Control of Reactor Vessel Water Level Switches
Control of Reactor Vessel Water Level Switches
LER
Missed Surveillances for Fire Protection Equipment
Missed Surveillances for Fire Protection Equipment
LER
Gross Analysis on Liquid Effluent Grab Samples
Gross Analysis on Liquid Effluent Grab Samples
Inadequate
Corrective Actions for Check Valve
Problems
50-387/97-07-08
50-388/97-03-01
50-388/97-03-03
CS chiller was Outside the Plant's Design Basis
Two Examples of an Inadequate
Procedure
Four Examples, Failure to Perform 50.59 Evaluation
~Udated
50-388/97-03-02
Core Spray System Surveillance Preconditioning
31
LIST OF ACRONYMS USED
CFR
CIG
CL
CR
ERT
IERP
LCO
LER
NRC
OP
PCO
SOOR
SPING
TBVS
TS
WA
Alarm Response
Code of Federal Regulations
Containment Instrument Gas
Check Lists
Condition Report
Control Room Emergency Outside Air Supply System
Diesel Generator
Event Review Team
Final Safety Analysis Report
Industry Event Review Program
Instrumentation and Controls
Limiting Conditions for Operation
Licensee Event Report
Nonconformance Report
Non-Cited Violation
Nuclear Plant Operator
Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Operating Experience Services
Operating Procedure
Plant Control Operator
Quality Assurance
Residual Heat Removal Service Water
Significant Operations Occurrence
Report
System Particulate Iodine Noble Gas
Susquehanna
Steam Electric Station
Turbine Building Ventilation Stack
Technical Specification
Updated Final Safety Analysis Report
Unreviewed Safety Question
Work Authorization