ML17164A956
| ML17164A956 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 01/26/1999 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17164A954 | List: |
| References | |
| 50-387-98-12, 50-388-98-12, NUDOCS 9902090347 | |
| Download: ML17164A956 (29) | |
See also: IR 05000387/1998012
Text
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket Nos:
License Nos:
50-387, 50-388
Report No.
50-387/98-1 2, 50-388/98-1 2
Licensee:
Pennsylvania Power and Light Company
2 North Ninth Street
Allentown, Pennsylvania
19101
Facility:
Susquehanna
Steam Electric Station
Location:
P.O. Box 35
Berwick, PA 18603-0035
Dates:
November 24, 1998 through January 4, 1999
Inspectors:
S. Hansell, Senior Resident Inspector
J. Richmond, Resident Inspector
A. Blarney, Resident Inspector
Approved by:
Clifford Anderson, Chief
Projects Branch 4
Division of Reactor Projects
9902090347 990i26
ADOCK 05000387
8
POR
EXECUTIVE SUMMARY
Susquehanna
Steam Electric Station (SSES), Units
1 5, 2
NRC Inspection Report 50-387/98-12, 50-388/98-12
This inspection included aspects of Pennsylvania Power and Light Company's (PPSL's)
operations, maintenance,
engineering,
and plant support at SSES.
The report covers a six-
week period of resident inspection.
~Oerations
The operator response to a Unit 1 loss of main condenser offgas system was
excellent.
Timely restoration of the offgas equipment by nuclear plant operators
enabled plant control operators to stabilize the plant in a safe condition.
(Section
01.1)
During a planned plant process computer outage, PPRL removed one of the two
methods being utilized to monitor suppression
pool average water temperature
and
disabled the initial suppression
pool water high temperature control room overhead
PPRL did not recognize that Unit 2 had entered
two limiting
conditions for operations.
This resulted in a violation of minor significance because
suppression
pool bulk temperature
did not exceed 90
F.
(Section 04.1)
In December 1998,'PPRL incorrectly implemented
a complex residual heat removal
service water system Technical Specification Interpretation (TSI). Previous to this
event in October, 1998, PP8cL did not implement this TSI due to a lack of a
reference to the TSI.
In both instances
PPSL returned the equipment to an operable
status within the required time limit specified in the TSI.
PP&L corrective actions
include planned revisions to the TSI and ultimately removal of all TSls.
(Section
03.1)
PPSL identified that channel functional surveillance tests of the source range
monitors did not include the indication portion of the channels
as acceptance
criteria, as required by Technical Specifications.
PPRL's proposed
and completed
corrective actions, including procedure and programmatic actions, were good.
This
non-repetitive, licensee identified and corrected violation is being treated as a non-
cited violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.
LER
50-387/388/98-017
is closed.
(Section 08.1)
Maintenance
~
Management's
decision to stroke the Unit 1 outboard main steam isolation valve
(MSIV), prior to the required surveillance test, was proactive and resolved a
potential safety problem that could have resulted in a higher than expected pressure
increase during a postulated MSIV closure event.
(Section M1.1)
Executive Summary (cont'd)
The Unit 2 high pressure coolant injection (HPCI) system outage was well planned
and executed.
The pump and turbine equipment areas were maintained as clean
areas which resulted in an excellent work environment.
Excellent coordination of
the HPCI post maintenance test minimized the heat addition to the suppression
pool.
(Section M1.1)
~
.
Instrumentation and control technicians promptly reported an activity that led to the
foreign material addition to the Unit 2 standby liquid control (SLC) tank.
The
technicians, actions were representative of a good safety culture to report work
activity problems.
The shift supervisor's continuous operability assessment
led to
the appropriate SLC pump operability determination and the timely removal of all
foreign material from the SLC tank.
(Section M1.1)
Encnineering
~
PPSL failed to adequately translate the system design, from a modification, into
appropriate specifications, drawings, and procedures,
and on two separate
occasions substituted gasket material without a review for suitability of materials.
The inspectors determined this was an apparent violation of 10 CFR 50 Appendix B,
Criterion III, Design Control. PP5L's initial corrective actions were good.
However,
the proposed final corrective actions, which appeared
reasonable to correct'the
original condition, were not performed in a timely manner.
In addition, PPSL failed
to recognize that SSES design control requirements
had not been followed, when a
different type gasket was installed in the plant.
URI 50-387,388/98-06-03
is
closed. (Section. E8.2)
~
System and maintenance
engineers provided good outage support at the high
pressure coolant injection (HPCI) jobsite.
Also, the HPCI system engineer monitored
the post maintenance
surveillance test and provided timely feedback to the operator
performing the test.
(Section M1.1)
Plant Su
ort
~
The security computer replacement,
in the Security Control Center, was well
controlled and completed with minimal interruptions to the normal plant access
. areas.
A significant improvement was noted for the plant accountability capabilities.
(Section S2)
TABLE OF CONTENTS
EXECUTIVE SUMMARY
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II
TABLE OF CONTENTS
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IV
Summary of Plant Status
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I. Operations
01
03
04
08
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Conduct of Operations
01.1
Unit Operations and Operator Activities
01.2
Operational Safety System Alignment
Operations Procedures
and Documentation .............
03.1
Technical Specification Operability Determinations...
Operator Knowledge and Performance
04.1
Suppression
Pool Bulk Water Temperature Monitoring
Miscellaneous Operations Issues
08.1
Licensee Event Report Review ~"................
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I. Maintenance
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M1
Conduct of Maintenance......
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M1.1
Surveillance and Pre-Planned
Maintenance ActivityReview
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E8
Miscellaneous Engineering Issues
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E8.1
Followup of Open Items
E8.2
"A" Emergency Diesel Generator Inoperable due to Heavy Rains ... 9
IV. Plant Support ............
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Status of Security Facilities and Equipment
V. Management Meetings
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Exit Meeting Summary
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1 1
ATTACHMENTS
Attachment
1 - Inspection Procedures
Used
- Items Opened, Closed, and Discussed
- List of Acronyms Used
Re ort Details
Summar
of Plant Status
Susquehanna
Steam Electric Station (SSES) Unit 1 maintained 100% power throughout the
inspection. period, except for the following power reductions.
On November 27, 1998,
power was reduced to 90% for approximately one hour due to electrical grid minimum load
considerations.
On December 11, power was reduced to 72% due to a load center
electrical breaker trip that resulted in an isolation of the main condenser offgas system.
On
December 13, 1998, reactor power was raised to 100% after restoration of the load center
trip and a completion of a control rod pattern sequence
exchange.
The unit remained at
100% for the rest of the inspection-period;
SSES Unit 2 maintained 100% power throughout the inspection period, except for the one
power reduction to 90% for approximately one hour due to electrical grid minimum. load
considerations
on November 27, 1998.
01
Conduct of Operations
'1.1
Unit 0 erations and 0 erator Activities
a.
Ins ection Sco
e 71707
Routine operations activities of plant control operators
(PCOs), nuclear plant
operators
(NPOs), unit supervisors
(USs), and shift supervisors
(SSs) were observed.
b.
Observations
and Findin s
The operator response to a Unit 1 loss of main condenser offgas system was
excellent.
The loss of the offgas system was due to a 480 Volt load center
electrical breaker trip related to the spurious trip of the breaker overcurrent
protection unit. Timely restoration of the offgas equipment by nuclear plant
operators enabled plant control operators to stabilize the plant at 72% reactor
power. After transfer of electrical loads to a backup power supply and completion
of additional planned activities, operators raised reactor power back to 100%.
The inspectors determined routine operator activities were adequately prescribed,
communicated,
and conservatively performed in accordance with SSES operations
department procedures.
Shift turnovers were observed to be detailed and complete.
The inspectors discussed plant conditions with PCOs and USs following shift
turnovers and observed sufficient information and status were transferred to the
oncoming shift to ensure the safe operation of the units.
The licensee was
I
'Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized reactor inspection report outline.
Individual reports are not expected to address all outline topics.
observed to conduct plant operations in accordance with procedures,
and effective
controls were implemented for safe plant operation.
C.
Conclusions
The operator response to a Unit 1 loss of main condenser offgas system was
excellent.
Timely restoration of the offgas equipment by nuclear plant operators
enabled plant control operators to stabilize the plant in a safe condition.
01.2
0 erational Safet
S stem Ali nment
(71707)
During plant tours, the alignment and operability of selected safety systems,
engineered safety features,
and on-site power sources were verified. A partial
walkdown of the following systems was performed:
Unit 2 Standby Liquid Control System
Unit Common Standby Gas Treatment System (SGTS)
Unit 1 Engineered Safety Features Instrument Racks
Emergency Service Water
Residual Heat Removal Service Water
Spent Fuel Pool Cooling Water
Overall equipment operability, material condition, and housekeeping
conditions were
good.
The inspectors identified several minor housekeeping
and material condition
items, including=seismically unrestrained equipment (used for charcoal filter
maintenance)
stored on top of the SGTS filter trains.
The items did not affect
system operability and were resolved satisfactorily.
03
Operations Procedures
and Documentation
03.1
Technical S ecification 0 erabilit
Determinations (71707,40500)
On October 27, 1998, the NRC identified that PP&L had inappropriately entered
a
30 day Limiting Condition for Operation (LCO) for planned maintenance
on the "1A"
residual heat removal service water (RHRSW) pump in accordance with technical
specification (TS) section 3.7.1.
TSs allow a 30 day LCO with one RHRSW
subsystem
Technical Specification Interpretation (TSI) 1-97-007,
reduces the LCO to 7 days because
TSs do not account for potential failures within
the RHRSW subsystem flow paths.
The Unit Supervisor (US) did not review the TSI
prior to implementing the LCO. PPRL exited the LCO within the required seven
days, as delineated by the TSI; initiated condition report (CR) 76161; and improved
the references to active TSls in the applicable TS sections.
This issue was
previously documented
in IR 50-387/98-11, 50-388/98-11.
On December 29, 1998, the NRC identified that PPSL had inappropriately entered
a
30 day LCO for planned maintenance
on the "2A" RHRSW pump in accordance with
TS section 3.7.1, instead of 'the 7 days allowed by TSI 2-97-007.
The US correctly
identified that TSI 1-.97-007 was applicable; however, due to the complexity of this
TSI, the US incorrectly interpreted the TSI.
PP&L exited the LCO within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,
initiated CR 87503, and plans to simplify the TSI.
In conclusion, in December 1998, PP&L incorrectly implemented
a complex residual
heat removal system Technical Specification Interpretation (TSI). Previous to this
event, in October, 1998, PP&L did not implement this TSI, due to a lack of a
reference to the TSI.
In both instances,
PP&L returned the equipment to an
operable status within the required time limit specified in the TSI.
PP&L corrective
actions include planned revisions to the TSI and, ultimately, removal of all TSls.
04
Operator Knowledge and Performance
04.1
Su
ression Pool Bulk Water Tem erature Monitorin
Ins ection Sco
e 71707
40500
The inspectors reviewed PP&L's method of monitoring suppression
pool average
temperature during a planned plant process computer (PICSY)'outage.
b.
Observations
and Findin s
On December 15, 1998, at 5:55 a.m., SSfS Unit 2 removed the PICSY computer
from service for planned maintenance.
This action removed one of two methods
being utilized to monitor suppression
pool average temperature
and disabled the
initial suppression
pool water high temperature control room overhead annunciator.
Suppression'Pool
Average Water Temperature Monitoring Requirements
TS 3.6.2.1 Suppression
Pool Average Water Temperature,
requires suppression
pool
average temperature to be verified less than 90'
once every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> during
normal operation.
If suppression
pool temperature
exceeds 90', TS 3.6.2.1.A.1
requires the average temperature to be verified less than 110'
hourly. Hourly is
considered
an adequate frequency due to redundant indication and alarms available
to alert the operator to abnormal suppression
pool average temperature conditions.
TS allows three methods for monitoring the suppression
pool average water
temperature.
The methods are (a) Suppression
Pool Temperature Monitoring
System (SPOTMOS), (b) plant process computer system (PICSY) calculation, or (c)
manual calculation, if there is no testing or transient that is adding heat to the
suppression
pool ~
When PP&L removed the PICSY computer from service on December 15, 1998,
SPOTMOS was the only real time indication of suppression
pool average water
temperature.
SPOTMOS indicated 99'
which was greater than the 84'
indicated by the PICSY computer prior to removing the PICSY computer from
service.
The SPOTMOS high temperature indication required the PCOs to monitor
suppression
pool average water temperature hourly, until the temperature was
reduced to less than 90'
(TS 3.6.2.1.A.1).
The Unit 2 US and PCOs did not
monitor the suppression
pool average temperature hourly nor did they perform a
manual calculation.
The inspectors discussed this issue with the Unit 2 US and
PCOs and at 8:40 a.m. operations completed
a manual calculation, allowed by TSs
and confirmed that suppression
pool average bulk water temperature was less than
90'. This calculation was completed in 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 45 minutes after the PICSY
computer was removed from service, which exceeded the hourly monitoring
requirements of TS 3.6.2.1.A.1.
Because the suppression
pool average bulk water
temperature
did not exceed 90', this failure constituted
a violation of minor
significance and is not subject to formal enforcement action.
Suppression
Pool First Level High Water Temperature Alarm
The TRM section 3.6.3, Suppression
Pool Alarm Instrumentation, requires that four
levels of alarms be operable to monitor suppression
pool water temperature.
If any
of the alarms becorn'e inoperable TRM 3.6.2.A.1 requires the alarm to be restored in
24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The PICSY computer provides the process input for the suppression
pool
first level high water temperature
alarm.
When the PICSY computer was removed
from service the first level alarm became inoperable.
This further degraded
information available to alert the operators of abnormal suppression
pool
temperature conditions.
The Unit 2 US did not identify and document this LCO.
However, this alarm was restored within the allowed 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
C.
Conclusions
During a planned plant process computer outage, PPKL removed one of the two
methods being utilized to monitor suppression
pool average water temperature
and
disabled the initial suppression
pool water high temperature control room overhead
PPRL did not recognize that Unit 2 had entered
two limiting
conditions for operations.
This resulted in a violation of minor significance because
suppression
pool bulk temperature
did not exceed 90 'F.
08
Miscellaneous Operations Issues
08.1
Licensee Event Re ort Review (71707,92700)
CLOSED
LER 50-388 98-009-00
Unit 2 "A" Moisture Se arator Drain Tank Hi h-Hi h Level Scram
On June 29, 1998, Unit 2 was conducting
a plant startup with reactor power at
55% power.
An unexpected
actual "A" moisture separator drain tank high-high
level was sensed
by four instruments in three independent instrument loops.
This
resulted in a main turbine trip and a subsequent
reactor scram.
Prior to the Unit 2
restart, the inspectors reviewed the preliminary root cause investigation, initial
corrective actions taken, condition reports and plant status.
The inspectors in field
review verified that the deficiencies were corrected, and General Operating (GO)
procedure GO-100/200-002 was revised to maintain the steam crossover pipe
drains open until 30% reactor power.
No violations of NRC requirements were
identified. This LER is closed.
Closed
LER 50-387 98-017-00 and LER 50-387 98-017-01
Incomplete Channel Functional Test of Source Range Monitor Channels
PP&L identified that channel functional surveillance testing of the source range
monitors (SRMs) did not include the channel indication acceptance
criteria, as
required by Technical Specifications (TSs).
The condition had existed since initial
plant operation, approximately 15 years.
Based on an in-field review of the issues reported in the licensee event report (LER),
TS, surveillance procedures,
and associated
corrective actions, the inspectors
confirmed that PP&L failed to adequately perform channel functional surveillance
testing of the SRMs, as required by TSs.
Although the SRM channel functional
surveillance tests, performed over an extended period, did not include test
acceptance
criteria for SRM indication, this did not represent
a repetitive condition,
because
it resulted from a single failure to originally establish an adequate
surveillance procedure.
Failure'to perform a channel functional surveillance testing
of the SRMs was of minor safety significance since periodic calibration of the SRMs
performed the same test.
The inspectors determined that PP&L properly identified
and reported this issue, and found PP&L's proposed and completed corrective
actions to be good.
In conclusion, in a Licensee Event Report, PP&L identified that channel functional
surveillance tests of the source range monitors did not include the indication portion
of the channels
as acceptance
criteria, as required by Technical Specifications.
PP&L's proposed and completed corrective actions, including procedure and
programmatic actions, were good.
This non-repetitive, licensee identified and
corrected violation is being treated as a non-cited violation, consistent with Section
VII.B.1 of the NRC Enforcement Policy. This LER is closed.
(NCV 50-387/98-12-
01)
II. Maintenance
M1
Conduct of Maintenance
M1.1
Surveillance and Pre-Planned
Maintenance Activit Review
a.
Ins ection Sco
e 61726 62707
The inspectors observed and reviewed selected portions of pre-planned maintenance
and surveillance activities, to determine whether the activities were conducted
in
accordance with NRC requirements
and SSES procedures.
Observations
and Findin s
Based on the indicated sample of safety related work authorizations and
surveillances, the inspectors found pre-planned maintenance
and surveillance
activities were appropriately conducted and controlled.
The sample included:
Work Authorizations
V82396
V82398
U86624
U66631
S83786
A83521
V82435
IS.C Support for Unit 2 Standby Liquid Control (SLC) Maintenance
Unit 2 SLC Storage Tank Foreign Material Removal
Post Modification Test for Reactor Water Cleanup (RWCU) Vibration
Alarm Removal (DCP 98-9005)
Post Modification Test for Rod Drift Memory Card (DCP 95-9053)
"1B" RHRSW Pump Overhaul
"B" Emergency Diesel Generator Fuel Oil Storage Tank Clean 5
Inspect
ISC Support for the Quarterly Turbine Valve Testing
Surveillances
SO-030-001
SO-030-003
SO-104-001
SO-21 6-003
SO-252-002
SO-293-001
SR-255-004
SO-256-001
TP-024-1 60
CREOASS Monthly Performance Test
Quarterly Control Structure Chilled Water Flow Verification
Monthly Bus 1A201, 1A202, 1A203, 1A204 and OB565 Degraded
Voltage Channel Functional Test
Quarterly RHRSW Flow Verification
Quarterly HPCI Flow Verification
Quarterly Turbine Valve Cycling
Unit 2 Scram Time Testing for Control Rod 30-03
Weekly Control Rod Exercising
"E" Diesel Generator Emergency Test
In addition, selected portions of procedures,
drawings, and vendor technical
manuals, associated with the maintenance
and surveillance activities, were also
reviewed and determined to be acceptable.
In general, maintenance
personnel were
very knowledgeable of their assigned
activities.'B"
Outboard Main Steam Isolation Valve (MSIV) Repair
The previous surveillance test (ST) for the "B" outboard MSIV, HV141F028B, noted
that the stroke time was shorter than previous trend data but within the Technical
Specification (TS) limits of 3 to 5 seconds.
Plant management
made a decision to
stroke the valve before the required quarterly surveillance due to the trend.
During a planned power reduction on December 12, 1998, the valve was tested and
stroked closed in 1.63 seconds.
Operations declared the valve inoperable and
entered the applicable TS limiting condition for operation (LCO). The maintenance
crew found and repaired the cause of the fast stroke time, a leaking oil plug on the
valve dashpot.
After the completed repairs, the valve was stroked close in 4.31
seconds
and declared operable.
Management's
decision to stroke the MSIV, prior to
the required ST, was proactive and resolved
a problem that could have resulted in a
higher than expected pressure
increase during a postulated MSIV closure event.
High Pressure
Coolant Injection (HPCI) System Outage
The Unit 2 high pressure, coolant injection (HPCI) system outage was well planned
and executed.
Maintenance worker performance and knowledge of the HPCI
system corrective and preventive maintenance tasks were good.
The pump and
turbine equipment areas were maintained as clean areas which resulted in an
excellent work environment.
System and component engineers were present at the
jobsite to provide support as needed.
Prior to the HPCI flow test surveillance, the unit supervisor (US) led a detailed pre-
evolution briefing to ensure the post maintenance testing (PMT) was completed as
required.
The briefing included plant operators, health physics, system engineering
and maintenance
personnel involved with the work activities.
An excellent
discussion resulted in a well coordinated plan to ensure all PMT activities were
verified. Plant control operators'est
performance and knowledge of the HPCI
operation were excellent.
Also, the HPCI system engineer monitored the post
maintenance
surveillance test and provided timely feedback to the operator
performing the test. The pump and turbine startup and flow test were controlled and
demonstrated
system operability. The work group's good coordination of the test
minimized the heat addition to the suppression
pool.
Standby Liquid Control'(SLC) Storage Tank Foreign Material Removal
During an Instrument and Control (I&C) monthly preventative maintenance
(PM)
activity, to clean the Unit 2 SLC storage tank level instrument bubbler tube, a
portion of an l&C cleaning tool (a 3 inch long piece of stainless wire) broke off inside
the tank.
The I&C technicians immediately reported the problem to operations.
The operations plant supervisor performed an internal tank visual inspection which
identified additional foreign material inside the tank (a 3 inch by 6 inch piece of cloth
caught on a support bolt for the air sparger).
The initial operability determinatio'n concluded that the foreign material inside the
tank would not float free or, become entrained in a SLC pump suction line.
However, based on a more detailed tank inspection, three days later, operations
concluded that the cloth was not "firmlyattached,"
and declared one train of SLC
The cloth, and the piece of wire, were promptly removed by
maintenance the next day.
The retrieval of the foreign material eliminated all SLC
system operability concerns.
C.
Conclusions
Management's
decision to stroke the MSIV, prior to the required ST, was proactive
and resolved a problem that could have resulted in a greater pressure
increase
during a postulated MSIV closure event.
The Unit 2 high pressure coolant injection (HPCI) system outage was well planned
and executed.
The pump and turbine equipment areas were maintained as clean
areas which resulted in an excellent-work environment.
Excellent coordination of
the HPCI post maintenance test minimized the heat addition to the suppression
pool ~
System and maintenance
engineers provided good outage support at the high
pressure coolant injection (HPCI) jobsite.
Also, the HPCI system engineer monitored
the post maintenance
surveillance test and provided timely feedback to the operator
performing the test.
Instrumentation and control technicians promptly reported an activity that led to the
foreign material addition to the standby liquid control (SLC) tank.
The
technicians'ctions
were representative
of a good safety culture to report work activity
problems.
The shift supervisor's continuous operability assessment
led to the
appropriate SLC pump operability determination and the timely removal of all foreign
material from the SLC tank.
III. En ineerin
E8
Miscellaneous Engineering Issues
E8.1
Followu
of 0 en Items (37551,92903)
Closed
VIO 50-387 388 98-08-02
Emergency Diesel Generator Day Tank Minimum Volume
In 1990 and 1991, PPSL identified that the fuel oil transfer pump automatic start
level switch setpoints for the emergency diesel generator day tanks did not meet the
American National Standards Institute (ANSI) requirements.
The ANSI requirement
to ensure
a day tank minimum fuel oil volume sufficient for 60 minutes of diesel
operation at the level where fuel oil is automatically added to the day tank was not
met.
PP&L documented this non-conforming condition, and implemented
administrative controls as compensatory
measures,
but failed to effect timely
resolution.
The failure to effect timely resolution was cited as a violation.
The inspectors performed an in-field review of PPRL's response to the violation,
Technical Specifications (TSs), and the final safety analysis report (FSAR).
PPRL's
corrective actions included a TS change request, submitted to the NRC on
November 20, 1998, and a design basis change which will resolve the non-
conforming condition.
The inspectors determined that
PPSL's corrective actions
were appropriate.
This violation is closed.
"A" Emer enc
Diesel Generator Ino erable due to Heav
Rains
Closed
URI 50-387 388 98-06-03
Ins ection Sco
e 37551 92903
On June 23, 1998, SSES experienced
heavy rains.
This resulted in water intrusion
into the "A" emergency diesel generator
(EDG) fuel oil storage tank.
This event was
reviewed in detail in NRC Inspection Report 50-387,388/98-06,
and identified as
Unresolved Item (URI) 50-387,388/98-06-03.
The inspectors reviewed PPRL's
corrective actions in response to this event.
Observations
and Findin s
In June, 1998, heavy rains resulted in significant quantities of water entering the
.
"A" emergency diesel generator
(EDG) fuel oil storage tank.
The rain water entered
the storage tank vault area immediately above the tank, in-part, through below
ground level unsealed penetrations into the vault. The vault penetrations were part
of an in progress modification, and had remained unsealed during the installation
work. The vault flooded to a depth of about five feet, and water leaked into the
.storage tank through a loose flange on the tank.
The consequences
of this event
resulted in the "A" EDG being inoperable for a short period of time, and in a
degraded condition for several days, following the event.
PPSL initiallydetermined that no programmatic or proceduie provisions existed to
require interim sealing of penetrations or breaches
into safety related structures or
barriers made during the course of modification or maintenance work, and is
continuing to evaluate foreign material exclusion program requirements.
PPSL
further determined the loose flange appeared to have resulted from gasket
deterioration, due to use of an incorrect gasket material (i.e., a rubber gasket
appeared to have been substituted for a neoprene gasket).
~
The inspectors performed an in-field review of PPSL's corrective actions,
which'ncluded
proposed field inspections of storage tank flange gaskets,
and proposed
procedure and programmatic changes.
PPSL's initial corrective actions were good,
and included immediate water removal from the fuel oil storage tank, inspection of
the other storage tanks and tank flanges, and sealing of the open penetrations into
the tank vault. The inspectors concluded the corrective actions, identified by
condition report (CR) 98-2183, appeared
reasonable to correct the condition and
prevent recurrence.
However, as of December 15, 1998, only one of the five
specified corrective actions had been completed.
Neither the corrective action to
determine the correct gasket material for the tank flanges, due by September 30,
1998, nor the corrective action to inspect all tank flange gaskets, for appropriate
gasket and replace as necessary,
due by October 30, 1998, had started,
as of
December 15, 1998.
The inspectors, therefore, concluded that the corrective
actions were not performed in a timely manner.
10
Confi uration of Fuel Oil Stora
e Tanks
A 1989 modification (PCN 89-9008) installed a different type of level instrument,
and added stilling wells to the storage tanks.
The function of the stilling well was
to provide a foreign material exclusion barrier, similar to a basket, for the level
instrument floats which hung inside the tank.
The stilling well was safety related,
while the instrument and floats were non-safety related.
The instrument/tank flange
is actually an assembly, consisting of three flanges sandwiched together by one set
of bolts (the bolts were designated
as safety related).
The lower gasket is between
the tank flange and the stilling well flange, and the upper gasket is between the
stilling well flange and the instrument flange.
Neoprene was specified for both
The inspectors determined that PPRL failed to revise design drawings (or other
appropriate design basis documents) to incorporate the design changes made by
modification 89-9008.
The unavailability of the design information for the correctly
specified gasket material resulted in the use of incorrect gasket material (i.e., rubber
instead of neoprene), which deteriorated due to exposure to fuel oil, and
subsequently
allowed water intrusion into the fuel oil storage tank on June 24,
'1998.
10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that
measures
be established to ensure that applicable regulatory requirements
and the
design basis are correctly translated into specifications, drawings, procedures
and
instructions.
The failure to adequately translate the system design, from a
modification, into appropriate specifications, drawings, and procedures
is an
example of an apparent violation of Appendix B Design Control requirements.
The inspectors found that on July 1, 1998, SSES maintenance
replaced the
instrument flange gasket, identified as having been deteriorated
and loose, with a
flexitalic gasket (i.e., different type of gasket).
The as-left condition was an upper
flange flexitalic gasket and a lower flange neoprene gasket, with the flange torqued
to the required value for the flexitalic. The applied torque greatly exceeded the
maximum allowed for the lower flange neoprene gasket.
PPRL has subsequently
determined that both the upper and lower gaskets must be of the same type.
As of
January 4, 1999, no operability determination, or condition report interim use-as-is
.or repair disposition had been performed to evaluate the as-left condition. Also, no
approval existed for the use of a flexitalic gasket as an alternate replacement item
for the as-found gasket.
The use of the flexitalic gasket, without the required SSES
evaluations and approvals, was identified by the NRC during the inspectors'eview
of CR 98-2183.
Although the CR did identify that a flexitalic gasket had been
installed by maintenance
in July, the CR did not identify or recognize the gasket
substitution as an action which was not performed in accordance with required
station procedures for operability determinations
and replacement item evaluations.
The NRC further identified that work order S83104, which installed the flexitalic
gasket, was designated
as non-safety related and non-ASME, which would have
allowed the use of non-safety related bolts on the flange.
Criterion III, Design Control, requires, in part, that measures
be established for the
selection and review for suitability of application of materials and parts.
The failure
11
of PPtkL to perform a replacement item evaluation, prior to substituting a flexitalic
gasket for a neoprene gasket is a second example of an apparent violation of
Appendix B Design Control requirements.
This URI is closed.
(VIO 50-387,388/98-
12-02)
c.
Conclusions
PPRL failed to adequately translate
a system design change into appropriate
specifications, drawings, and procedures,
and on two separate
occasions
substituted gasket material without a review for suitability of materials.
PPSL
determined that the use of an incorrect gasket material was a root cause for
significant water intrusion into an emergency diesel fuel oil storage tank on June 24,
1998.
The inspectors determined this was an apparent violation of 10 CFR 50
Appendix B, Criterion III, Design Control.
PP&L's initial corrective actions were
good.
However, the proposed final corrective actions, which appeared
reasonable
to correct the original condition, were not performed in a timely manner.
In
addition, the NRC identified that PPSL failed to recognize that SSES design control
requirements
had not been followed when a different type of gasket was installed
on July 1, 1998.
This URI is closed.
IV. Plant Su
ort
S2
Status of Security Facilities and Equipment
(71750,92904)
The secunty computer replacement,
in the Secunty Control Center, was well
controlled and completed with minimal interruptions to the normal plant access
areas.
The inspectors also verified, through observations
and interviews, that the
computer replacement modification did not interfere with operational activities, or
the execution of the detection, assessment
and response functions.
A significant
improvement was noted for the plant accountability
capabilities.'.
Mana ement Meetln s
Xl
Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management
at the conclusion of the inspection report period on January 11, 1999.
The licensee
acknowledged the findings presented.
The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary.
No proprietary information was
identified.
ATTACHMENT1
INSPECTION PROCEDURES USED
IP 37551
IP 61726
IP 71707
IP 92901
Engineering
Onsite Engineering Observations
Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing
Problems
Surveillance Observations
Maintenance Observations
Plant Operations
On Site Followup of Reports
Followup Plant Operations
Followup Engineering
ITEMS OPENED, CLOSED, AND DISCUSSED
~Oeoed
50-387,388/98-1 2-02
"A" Emergency Diesel Generator Inoperable due to
Heavy Rains (Section E8.1)
50-387/98-1 2-01
I
Closed
50-388/98-009-00
Incomplete Channel Functional Test of Source Range
Monitor Channels (Section 08.1)
LER
Unit 2 "A" Moisture Separator Drain Tank High-High
Level Scram (Section 08.1)
50-387/98-01 7-00
50-387/98-01 7-01
LER
Incomplete Channel Functional Test of Source Range
Monitor Channels (Section 08.1)
50-387,388/98-08-02
Emergency Diesel Generator Day Tank Minimum Volume
(Section E8.2)
50-387,388/98-06-03
"A" Emergency Diesel Generator Inoperable due to
Heavy Rains (Section E8.1)
Attachment
1
LIST OF ACRONYMS USED
ANSI
CFR
CR
DCP.
GDC
gpfn
IR
LCO
LER
NRC
PCO
TS
US
WA
American National Standards
Institute
American Society of Mechanical Engineers
Auxiliary Systems Operator
Boiling Water Reactor
Code of Federal Regulations
Condition Report
Control Room Emergency Outside Air Supply System
Design Change Package
Emergency Service Water
Fuel Pool Cooling
Final Safety Analysis Report
General Design Criteria
gallons per minu'te
,High Pressure
Coolant Injection
Hydrogen Water Chemistry
Instrument and Control
[NRC] Inspection Report
Inservice Testing
Improved Technical Specification
Limiting Condition for Operation
Licensee Event Report
Non-Cited Violation
Nuclear Plant Operator
Nuclear Regulatory Commission
Plant Control Operator
Reactor Building
Standby Liquid Control System
Senior Reactor Operator
Shift Supervisor
Susquehanna
Steam Electric Station
Technical Specification
Technical Specification Interpretation
[NRC] Unresolved Item
Unit Supervisor
Violation
Work Authorization
0