ML13226A255

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IR 05000482-13-003, 03/31 - 06/30/2013, Wolf Creek Generating Station, Integrated Resident and Regional Report; Inservice Inspection Activities, Follow-up of Events and Notices of Enforcement Discretion, Other Activities
ML13226A255
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 08/14/2013
From: O'Keefe N
NRC/RGN-IV/DRP/RPB-B
To: Matthew Sunseri
Wolf Creek
References
EA-13-084 IR-13-003
Download: ML13226A255 (90)


See also: IR 05000482/2013003

Text

UNITE D S TATE S

NUC LEAR RE GULATOR Y C OMMI S SI ON

R E G IO N I V

1600 EAST LAMAR BLVD

AR L I NGTON , TEXAS 7 60 11 - 4511

August 14, 2013

EA-13-084

Matthew W. Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

SUBJECT: WOLF CREEK GENERATING STATION - INTEGRATED INSPECTION

REPORT NO. 05000482/2013003, NRC INVESTIGATION REPORT 4-2012-023,

AND NOTICE OF VIOLATION

Dear Mr. Sunseri:

On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

the Wolf Creek Generating Station. In addition, the NRC Office of Investigations, Region IV

completed an investigation on March 28, 2013. The purpose of the investigation was to

determine whether an individual, formerly employed by Wolf Creek Generating Station, falsified

procedure paperwork. The enclosed inspection report documents the inspection results which

were discussed on July 11, 2013, with Mr. J. Broschak, Vice President of Engineering, and

other members of your staff. A supplement exit was conducted on August 7, 2013, with Mr. R.

Smith, Site Vice President and Chief Nuclear Operations Officer.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection and the information developed during the investigation,

the NRC has determined that a violation of NRC requirements occurred (EA-13-084). The

violation is cited in the enclosed Notice of Violation (Notice) and the circumstances surrounding

it are described in detail in the subject inspection report. Because the violation is associated

with willfulness, it was evaluated under the traditional enforcement process as set forth in the

NRC Enforcement Policy. The NRC concluded that the violation, absent willfulness, would be

considered a minor violation because the failure to complete and document the inspection per

the procedure did not have any safety significance.

However, the NRC considers the violation to have been more significant than minor, because it

involved willfulness, and therefore, the NRC has classified the violation at Severity Level IV, in

accordance with the NRC Enforcement Policy. The current Enforcement Policy is included on

the NRC's Web site at (http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html).

M. Sunseri -2-

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. If you have additional information that you

believe the NRC should consider, you may provide it in your response to the Notice. The NRC

review of your response to the Notice will also determine whether further enforcement action is

necessary to ensure compliance with regulatory requirements.

In addition, three NRC identified and two self-revealing findings of very low safety significance

(Green) were identified during this inspection. Each of these findings was determined to involve

violations of NRC requirements. Additionally, the NRC has determined that a traditional

enforcement Severity Level IV violation occurred. This traditional enforcement violation was

identified without an associated finding. The NRC is treating the NRC identified and self-

revealing findings as non-cited violations (NCVs), consistent with Section 2.3.2 of the

Enforcement Policy. These NCVs are described in the subject inspection report.

If you contest the violation or the significance of these NVCs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United

States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at Wolf Creek Generating Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at

Wolf Creek Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosures, and your response, if you choose to provide one, will be available electronically for

public inspection in the NRC Public Document Room or from the Publicly Available

Records (PARS) component of NRC's Agencywide Document Access and Management

System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room). To the extent possible, your response

should not include any personal privacy or proprietary, information so that it can be made

available to the Public without redaction.

Sincerely,

/RA/

Neil O'Keefe, Chief

Project Branch B

Division of Reactor Projects

Docket No.: 50-482

License No: NPF-42

M. Sunseri -3-

Enclosures:

1. Notice of Violation

2. Inspection Report 05000482/2013003

w/Attachments:

1. Supplemental Information

2. Information Request for Inspection Activities, documented in 71111.08

3. Information Request for Inspection Activities, documented in 71124.01

cc w/encl:

Electronic Distribution for Wolf Creek Generating Station

ML13226A255

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials NFO

Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials NFO

SRI:DRP/B RI:DRP/B SPE:DRP/B C:DRS/TSB C:DRS/EB1 C:DRS/EB2

CPeabody CHunt MBloodgood RKellar TFarnholtz GMiller

/RA/TFarnholtz

/RA/E /RA/E /RA/ /RA/ /RA/

for

08/05/13 08/12/13 08/13/13 08/07/13 08/07/13 08/09/13

C:DRS/OB C:DRS/PSB1 C:DRS/PSB2 C:ORA/ACES RC BC:DRP/B

VGaddy MHaire JDrake HGepford KFuller NOkeefe

/RA/for /RA/ /RA/ /RA/ /RA/E /RA/

08/07/13 08/07/13 08/08/13 08/13/13 08/08/13 08/13/13

NOTICE OF VIOLATION

Wolf Creek Nuclear Operating Corporation Docket No. 50-482

Wolf Creek Generating Station License No. NFP-42

EA-13-084

During an NRC inspection conducted on June 30, 2013, and an NRC investigation completed

on March 28, 2013, a violation of NRC requirements was identified. In accordance with the

NRC Enforcement Policy, the violation is listed below:

10 CFR 50.9 requires, in part, that information required by statute, orders, or license

conditions to be maintained by the licensee shall be complete and accurate in all

material respects.

Wolf Creek License Condition 2.C.5, Fire Protection, requires that the licensee shall

maintain in effect all provisions of the approved fire protection program as described in

the Standardized Nuclear Unit Power Plant System Final Safety Analysis Report.

Section 9.5-1 of the Wolf Creek Updated Final Safety Analysis Report, dated

March 10, 2013, describes the fire protection program and includes the licensees

commitment to meet Appendix 3A, Conformance to NRC Regulatory Guides, and

Appendix A, Table 9.5A-1 of Regulatory Guide1.39, Housekeeping Requirements for

Water-Cooled Nuclear Power Plants, Revision 2. Regulatory Guide 1.39, Revision 2,

endorses ANSI Standard N45.2.3-1973, Housekeeping During the Construction Phase

of Nuclear Power Plants.

ANSI Standard N45.2.3-1973, Section 3.5, states, in part, that periodic inspection and

examination of the work areas shall be performed at scheduled intervals to assure

adequacy of cleanliness and housekeeping practices. Section 4 of the above ANSI

Standard states, in part, that copies of inspection and examination records shall be

prepared and placed with other project records.

Section 6.1.8 of Procedure AP 12-001, Housekeeping Control, Revisions 6C and 7,

dated May 5, 2006, and November 10, 2008, respectively, intended to implement the

inspection and examination requirements of ANSI Standard N45.2.3-1973, states, in part

that assigned personnel shall walk down their areas monthly and that personnel

record and document their walkdowns using the Housekeeping Inspection Card.

Contrary to the above, between October and December 2008, the licensee failed to

maintain records required by License Condition 2.C.5 that were complete and accurate

in all material respects. Specifically, the Housekeeping Inspection Card for the spent

fuel pool area indicated that the inspection had been completed by a certain individual.

Security access logs, however indicated that the individual that completed the record

(Housekeeping Inspection Card) had not entered the area. This information is material

because it provides assurance to the NRC that the licensee has performed periodic

inspection and examination of work areas at scheduled intervals to assure adequacy of

cleanliness and housekeeping practices as required by the license condition.

-1- Enclosure 1

This is a Severity Level IV violation. (Section 6.9)

Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Corporation is

hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the

Regional Administrator, Region IV, and a copy to the NRC Resident Inspector at the Wolf Creek

facility within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This

reply should be clearly marked as a "Reply to a Notice of Violation; EA-13-084" and should

include for each violation: (1) the reason for the violation, or, if contested, the basis for disputing

the violation or severity level, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will

be achieved. Your response may reference or include previous docketed correspondence, if

the correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs Agencywide Documents and Access Management

System (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html, to the extent possible, it should not include any personal privacy, proprietary, or

safeguards information so that it can be made available to the public without redaction. If

personal privacy or proprietary information is necessary to provide an acceptable response,

then please provide a bracketed copy of your response that identifies the information that

should be protected and a redacted copy of your response that deletes such information. If you

request withholding of such material, you must specifically identify the portions of your response

that you seek to have withheld and provide in detail the bases for your claim of withholding (e.g.,

explain why the disclosure of information will create an unwarranted invasion of personal

privacy or provide the information required by 10 CFR 2.390(b) to support a request for

withholding confidential commercial or financial information). If safeguards information is

necessary to provide an acceptable response, please provide the level of protection described

in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 13th day of August, 2013

-2- Enclosure 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000482

License: NPF-42

Report: 05000482/2013003

Licensee: Wolf Creek Nuclear Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane NE, Burlington, Kansas

Dates: March 31 through June 30, 2013

Inspectors: C. Peabody, Senior Resident Inspector

C. Hunt, Acting Resident Inspector

M. Bloodgood, Senior Project Engineer

R. Kopriva, Senior Reactor Inspector

L. Ricketson P.E., Senior Health Physicist

B. Correll, Reactor Inspector

J. ODonnell, Health Physicist

C. Speer, Reactor Inspector

M. Williams, Reactor Inspector

Approved By: Neil O'Keefe, Chief, Project Branch B

Division of Reactor Projects

-1- Enclosure 2

SUMMARY OF FINDINGS

IR 05000482/2013003, 03/31 - 06/30/2013, Wolf Creek Generating Station, Integrated Resident

and Regional Report; Inservice Inspection Activities, Follow-up of Events and Notices of

Enforcement Discretion, Other Activities.

The report covered a 3-month period of inspection by resident inspectors and announced

baseline inspections by region-based inspectors. Five Green non-cited violations of significance

were identified. One Severity Level IV violation was identified. The significance of most

findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined

using Inspection Manual Chapter 0310, Components Within the Cross-Cutting Areas.

Findings for which the significance determination process does not apply may be Green or be

assigned a severity level after NRC management review. The NRC's program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, which states,

in part, activities affecting quality shall be prescribed by procedures of a type

appropriate to the circumstances and accomplished in accordance with these

procedures. Contrary to the above, the licensee failed to ensure procedures

related to the boric acid corrosion control program were adequate and properly

implemented. Specifically, prior to February 19, 2013, the licensee failed to:

(1) resolve discrepancies within the boric acid corrosion control program

procedure; (2) resolve discrepancies between the boric acid corrosion control

program procedure and the boric acid leak management procedure; and

(3) failed to track and resolve leakage for locations where health physics had

installed drip catch containments, to review the Health Physics Drip Bag Log as

part of the quarterly outside containment walkdown, and to add component

locations to the program. Further, the licensee failed to periodically assess the

effectiveness of the program on a refueling frequency. The violation was entered

into the licensees corrective action program as Condition Report 65212.

The inspectors determined that the failure to recognize discrepancies between

boric acid control procedures and the failure to follow boric acid program

procedures was a performance deficiency. The performance deficiency was

more than minor because it affected the Initiating Events Cornerstone attribute of

procedure quality and affected the cornerstone objective to limit the likelihood of

those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations, and if left uncorrected, the

performance deficiency had the potential to lead to a more significant safety

concern. Specifically, failure to resolve discrepancies within procedures or track

-2- Enclosure 2

and resolve leak locations where health physics had installed drip catch

containments had the potential to mischaracterize leaks or allow leaks to corrode

safety-related systems. Using Inspection Manual Chapter 0609, Appendix A,

The Significance Determination Process for Findings At-Power, the finding was

determined to be of very low safety significance (Green), because the finding

was a procedure quality problem that did not represent a loss of system safety

function, and did not screen as potentially risk significant due to a seismic,

flooding, or severe weather initiating event. The finding had a cross-cutting

aspect in the area of human performance associated with the work practices

component because the licensee failed to ensure supervisory and management

oversight of work activities, including procedure appropriateness and compliance,

such that nuclear safety is supported H.4(c) (Section 1R08.3.b.1).

  • Green. The inspectors identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, which states, in part, Measures

shall be established to assure that conditions adverse to quality are promptly

identified and corrected. Contrary to the above, the licensee failed to identify

and correct a condition adverse to quality in a timely manner. Specifically, prior

to February 19, 2013, the licensee failed to document the large area of boric acid

leakage and corroded steel plates on the south primary shield wall of the

containment refueling pool. The violation was entered into the licensees

corrective action program as Condition Report 64213.

The inspectors determined that the failure to promptly identify and evaluate a

condition adverse to quality was a performance deficiency. The performance

deficiency was more than minor because it affected the Initiating Events

Cornerstone attribute of human performance and affected the cornerstone

objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations,

and if left uncorrected, the performance deficiency had the potential to lead to a

more significant safety concern. Specifically, failure to implement corrective

actions could result in increased leakage and further degradation of the safety

system. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the inspectors determined that this finding was of

very low safety significance (Green), because it was not a design or qualification

deficiency, did not represent a loss of system safety function, and did not screen

as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. The finding had a cross-cutting aspect in the area of

human performance associated with the work practices component because the

licensee failed to define and effectively communicate expectations regarding

procedural compliance and that personnel follow procedures H.4(b)

(Section 1R08.3.b.2).

5.4.1.a was identified for failure to properly update operating procedures and

train operators on the effects of a recently installed modification. Specifically,

procedures were not adequately revised to provide guidance for operating the

-3- Enclosure 2

new Westinghouse Ovation digital turbine controls. As a result, operators shifted

operating modes at a power level that caused an 11 percent power increase due

to the combined characteristics of the steam control valves and the turbine

control unit. Additionally, operators were trained to shift control modes at low

power levels, where minor transients occurred, but were not restricted from

performing the shift at high power levels, where the transient could be more

significant. This issue was entered into the licensees corrective action program

under Condition Report 68711.

Failure to update station operating procedures to provide adequate guidance for

design changes, and failure to adequately train operators on those implemented

design changes is a performance deficiency. The performance deficiency is

more than minor because it affected the design control, procedure quality, and

human performance attributes of the Initiating Events cornerstone objective to

limit the likelihood of events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Using Inspection

Manual Chapter 0609, Appendix A, Checklist 1, Initiating Events Screening

Questions, the inspectors determined that the finding was of very low safety

significance (Green) because the finding did not result in a reactor trip coincident

with the loss of mitigation equipment. The inspectors determined that this finding

had a cross-cutting aspect in the area of human performance area of work

control, because the licensee did not appropriately communicate and coordinate

during activities in which interdepartmental coordination was necessary to assure

plant and human performance. Specifically, Wolf Creek did not communicate

and coordinate to ensure that procedure guidance and operator training

adequately conveyed the operational impacts of shifting turnine control modes at

different power levels H.3(b) (Section 4OA3.5.b.1).

  • Green. Inspectors identified a Green non-cited violation of Technical

Specification 5.4.1.a for the failure to follow Conduct of Operations and Reactivity

Management procedures. The inspectors reviewed an unplanned 11 percent

power increase during a shift in turbine control modes, and identified that pre-job

briefings did not adequately discuss expected plant response, operators did not

take action to limit the power increase when an unexpected response was

observed, and management was not adequately involved in decision making

prior to continuing power ascension before the details of an apparent turbine

control malfunction were fully understood. This issue was entered into the

licensees corrective action program under Condition Report 68711.

Failure to provide contingency actions for a greater than anticipated reactor

transient in the pre-job reactivity brief, and continuing with power ascension

without understanding the cause of the unexpected turbine control system

behavior is a performance deficiency. The performance deficiency is more than

minor because it affected the human performance attributes of the Initiating

Events cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Using Inspection Manual Chapter 0609 Appendix A, Checklist 1,

-4- Enclosure 2

Initiating Events Screening Questions, and the inspectors determined that the

finding was of very low safety significance (Green) because the finding did not

result in a reactor trip coincident with the loss of mitigation equipment. The

inspectors determined that this finding had a cross-cutting aspect in the area of

human performance area of work practices because the licensee failed to

communicate human error prevention techniques, such as holding pre-job

briefings, self and peer checking, and proper documentation of activities such

that work activities were performed safely. In addition, personnel proceeded in

the face of uncertainty or unexpected circumstances. Specifically, in the first

example control room operators pre-job reactivity brief was not appropriate

commensurate with the risk of the assigned task; in the second example station

personnel proceeded in the face of uncertainty H.4(a) (Section 4OA3.5.b.2).

Cornerstone: Mitigating Systems

Criterion XVI, Corrective Action, was identified on March 13, 2013. Specifically,

the licensee replaced a jacket water pressure transmitter ten times, but failed to

correct pressure oscillations that caused a fatigue failure of a pressure switch

diaphragm, which rendered emergency diesel generator B inoperable. The

inspectors concluded that the licensee ineffectively focused on correcting the

apparent source of the pressure oscillations, but failed to evaluate the effects of

the pressure cycles on components exposed to the same oscillations. This issue

was entered into the licensees corrective action program as Condition

Report 65624.

Failure to analyze the effects of pressure oscillations in the emergency diesel

jacket water system on interfacing system components is a performance

deficiency. The performance deficiency is more than minor because it affected

the equipment performance attribute of the Mitigating Systems cornerstone

objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. Using

Inspection Manual Chapter 0609 Appendix A, Significance Determination

Process for Findings At Power, and determined that the finding screens as very

low safety significance (Green) because the finding does not meet any criteria

outlined in the Exhibit 2, Section A. Specifically the finding did not represent a

loss of system safety function and did not exceed its technical specification

allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The inspectors determined that the finding had

a cross-cutting aspect in the area of problem identification and resolution

evaluations because the licensee failed to ensure that issues that potentially

affect nuclear safety are fully evaluated and addressed in a timely manner

P.1(c) (Section 4OA3.3).

-5- Enclosure 2

Cornerstone: Barrier Integrity

Completeness and accuracy of information, for the Wolf Creek Nuclear

Generating Stations failure to maintain complete and accurate records required

by a license condition. Title 10 CFR 50.9 requires, in part, that information

required by statute, orders, or license conditions to be maintained by the licensee

shall be complete and accurate in all material respects. Contrary to the above,

between October and December 2008, the licensee failed to maintain records

required by License Condition 2.C.5 that were complete and accurate in all

material respects. Specifically, the Housekeeping Inspection Card for the spent

fuel pool area indicated that the inspection had been completed when security

access logs indicate that the individual that completed the record had not entered

the area. The NRC investigation determined that the assigned individual did not

walk down the assigned area, and did not assign a designee to do so

(EA-13-084).

The failure to maintain records required by License Condition that are complete

and accurate in all material respects in accordance with 10 CFR 50.9 was a

violation. Because the violation is associated with willfulness and impacted the

regulatory process it was evaluated under the traditional enforcement process as

set forth in the NRC Enforcement Policy. Since this violation was the result of a

willful action, the NRC considers the violation to be more than minor, and

therefore, the NRC has classified the violation at Severity Level IV, in accordance

with the NRC Enforcement Policy (Section 4OA5).

B. Licensee-Identified Violations

None

-6- Enclosure 2

PLANT STATUS

The inspection period began with the unit in Mode 5 (cold shutdown) coming back from a

refueling outage in progress. The plant started up on April 13, 2013, and reached 100 percent

power on April 19, 2013. On April 29, 2013, the unit reduced power and the turbine was taken

off line to repair a stator cooling water leak. The turbine was restarted on May 2, 2013, the

same day the reactor experienced an unplanned transient (11percent power increase) while

shifting operating modes in the turbine steam controls. The unit returned to 100 percent power

on May 3, 2013. On May 7, 2013, the unit conducted a technical specification-required

shutdown due to a non-functional Class 1E air conditioner, and achieved cold shut down for

repairs the following day. The unit was restarted on May 13, 2013, and reached 100 percent

power on May 15. On June 17, 2013, the recently repaired Class 1E air conditioner showed

signs of substantial internal degradation. The unit began a technical specification-required

shutdown, reaching 16 percent power before the licensee was granted a Notice of Enforcement

Discretion to allow 7 days to replace the air conditioner again. Power was restored to

100 percent on June 19, 2013.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for June 27, 2013, the inspectors reviewed the plant personnels overall

protection for the expected weather conditions. On June 28, 2013, the inspectors

walked down the main transformer system because the oil cooling pumps circuit breaker

had tripped in the previous nights electrical storm, possibly due to lightning in the

vicinity. The inspectors evaluated the plant staffs recovery actions against the sites

procedures to verify whether the staffs actions were adequate. During the inspection,

the inspectors focused on plant-specific design features and the licensees procedures

used to respond to specified adverse weather conditions. The inspectors also toured the

plant grounds to look for any loose debris that could become missiles during a

subsequent storm. The inspectors evaluated operator staffing and accessibility of

controls and indications for those systems required to control the plant. Additionally, the

inspectors reviewed the Updated Safety Analysis Report and performance requirements

for the systems selected for inspection, and verified that operator actions were

appropriate as specified by plant-specific procedures. The inspectors also reviewed a

sample of corrective action program items to verify that the licensee-identified adverse

weather issues at an appropriate threshold and dispositioned them through the

corrective action program in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the attachment.

-7- Enclosure 2

These activities constitute completion of one adverse weather sample as defined in

Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Safety Analysis Report, technical specification requirements,

administrative technical specifications, outstanding work orders, condition reports, and

the impact of ongoing work activities on redundant trains of equipment in order to identify

conditions that could have rendered the systems incapable of performing their intended

functions. The inspectors also inspected accessible portions of the systems to verify

system components and support equipment were aligned correctly and operable. The

inspectors examined the material condition of the components and observed operating

parameters of equipment to verify that there were no obvious deficiencies. The

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the corrective action program with

the appropriate significance characterization. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of three partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

-8- Enclosure 2

.2 Complete Walkdown

a. Inspection Scope

On April 30, 2013, the inspectors performed a complete system alignment inspection of

the diesel generator B starting air system to verify the functional capability of the system.

The inspectors selected this system because it was considered both safety significant

and risk significant in the licensees probabilistic risk assessment. The inspectors

inspected the system to review mechanical and electrical equipment lineups, electrical

power availability, system pressure and temperature indications, as appropriate,

component labeling, component lubrication, component and equipment cooling, hangers

and supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. The inspectors reviewed a sample of

past and outstanding work orders to determine whether any deficiencies significantly

affected the system function. In addition, the inspectors reviewed the corrective action

program database to ensure that system equipment-alignment problems were being

identified and appropriately resolved. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • April 24, 2013, diesel generator B room, fire area D-1

centrifugal charging, and containment spray pump rooms), fire area A-4

  • May 20, 2013, Class 1E 4kV switchgear B room, fire area C-10
  • May 28, 2013, control room air conditioning room B, fire area A-21
  • May 28, 2013, control room air conditioning room A, fire area A-22

-9- Enclosure 2

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

.2 Annual Fire Protection Drill Observation (71111.05A)

a. Inspection Scope

On April 11, 2013, the inspectors observed a fire brigade activation response to an

actual fire near the auxiliary boiler exhaust stack. The observation evaluated the

readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee

staff identified deficiencies, openly discussed them in a self-critical manner, and took

appropriate corrective actions. Specific attributes evaluated were (1) proper wearing of

turnout gear and self-contained breathing apparatus; (2) proper use and layout of fire

hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient firefighting

equipment brought to the scene; (5) effectiveness of fire brigade leader communications,

command, and control; (6) search for victims and propagation of the fire into other plant

areas; and (7) utilization of preplanned strategies.

These activities constitute completion of one annual fire-protection inspection sample as

defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

- 10 - Enclosure 2

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records for the

essential service water (ESW)/service water macro foul treatment on June 12, 2013.

The inspectors verified that performance tests were satisfactorily conducted for heat

exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the

periodic maintenance method outlined in Electric Power Research Institute (EPRI)

Report NP 7552, Heat Exchanger Performance Monitoring Guidelines; the licensee

properly utilized biofouling controls; the licensees heat exchanger inspections

adequately assessed the state of cleanliness of their tubes; and the heat exchanger was

correctly categorized under 10 CFR 50.65, Requirements for Monitoring the

Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed

during this inspection are listed in the attachment.

These activities constitute completion of one annual heat sink inspection sample as

defined in Inspection Procedure 71111.07-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08)

Completion of Sections .1 through .5, below, constitutes completion of one sample as

defined in Inspection Procedure 71111.08-05.

.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control

(71111.08-02.01)

a. Inspection Scope

The inspectors observed 16 nondestructive examination activities and reviewed

two nondestructive examination packages that included five types of examinations.

The inspectors directly observed the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Main Steam Report # MT3954: Feedwater heater Magnetic Particle

flange, Work Package # 13-364385-000,

Drawing # M-010A-0054

Essential Service Report # MT3964, Work Order 11- Magnetic Particle

Water 341145-000, Drawing EFV0062, RHR

- 11 - Enclosure 2

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

pump room B, ESW valve EFV00062

Essential Service Report # MT3963, Work Order 11- Magnetic Particle

Water 340718-002, Drawing EFV0061, RHR

pump room B, ESW valve EFV00061

Reactor Coolant Report # 3705, Work Order 11-339304- Penetrant

System 005, Weld ID# W1A

Safety relief valve drain line valve

BBV0088

Reactor Coolant Report # 3606, Work Order 11-339304- Penetrant

System 005, Drawing # M-13BB13

Safety relief valve drain line valve

BBV0085

Reactor Coolant Report # 4236- Work Order 11-339304- Radiograph

System 005, ID # W-2A, Reactor pressurizer

safety relief valve drain line valve

BBV0088

Reactor Coolant Report # 4235, Work Order 11-339208- Radiograph

System 006, ID # W-3A , Reactor pressurizer

safety relief valve drain line valve

BBV0085

Reactor Coolant Report # RF19 JEW-004. Longitudinal Ultrasonic

System seam weld on reactor pressurizer (shell

to shell weld). ISI # TBB03-SEAM-1-W

Reactor Coolant Report # RF19-JLD-001. Examination of Ultrasonic

System weld overlay on reactor pressurizer

surge line (including both the nozzle to

safe-end dissimilar metal weld and the

safe-end to pipe stainless steel weld).

ISI #TBB03-MW7090-WOL-DM and #

TBB03-MW7090-WOL-SS.

Reactor Coolant Report # RF19 GPF-004. Reactor Ultrasonic

System pressurizer surge nozzle inner radius

examination. ISI # TBB03-10A-IR.

Reactor Coolant Report # RF19-JEW-005. Reactor Ultrasonic

System pressurizer surge nozzle to shell weld.

ISI # TBB03-10A-W

Main Steam Report # RF19-GPF-005. 28 inch Fluted Ultrasonic

Head to Pipe. ISI # AB-01-F050, Loop 3

Circumferential Weld.

- 12 - Enclosure 2

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Reactor Coolant Work Order 339304-005, ID # W-1A and Visual

System W-4A, Safety relief valve drain line valve

BBV0088

Reactor Coolant Work Order 339304-000, ID # W-1B Visual

System and W-4A, Safety relief valve drain line

valve BBV0085

Main Steam Work Order 11-344165-005 Visual

ID # AB-01-C011, Room 1412 Area 5,

Support and hanger

Main Steam Work Order 11-344165-005 Visual

ID # AB-01-H005, Room 1412 Area 5,

Piping Support

The inspectors reviewed records for the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Reactor Coolant Work Order 339304-000, ID # W-2 and Visual

System W-3A, Safety relief valve drain line valve

BBV0085

Reactor Coolant Work Order 339304-005, ID # W-2B and Visual

System W-3, Safety relief valve drain line valve

BBV0088

During the review and observation of each examination, the inspectors verified that

activities were performed in accordance with the American Society of Mechanical

Engineers (ASME) Code requirements and applicable procedures. There were no

relevant conditions identified for ASME Code Class 1 and 2 systems since the beginning

of the last refueling outage. The inspectors also verified that the qualifications of

nondestructive examination technicians performing the inspections were current.

The inspector observed the following welding activities:

SYSTEM WELD IDENTIFICATION WELD TYPE

Reactor Coolant Work Order 339304-000, ID # W- Tungsten Inert Gas

System 1B and W-4A, Safety relief valve Welding (GTAW)

drain line valve BBV0085

Reactor Coolant Work Order 339304-005, ID # W- Tungsten Inert Gas

System 1A and W-4A, Safety relief valve Welding (GTAW)

drain line valve BBV0088

- 13 - Enclosure 2

Essential Service RHR pump room, ESW room Tungsten Inert Gas

Water cooler valve replacement. Valve Welding (GTAW)

EFV0061, Work Order 11-34018-

002, Drawing # M-13EF04, ID #

PW-1A and PW-2A

Essential Service RHR pump room, ESW room Tungsten Inert Gas

Water cooler valve replacement. Valve Welding (GTAW)

EFV0062, Work Order 11-34145-

000, Drawing # M13EF05. ID #

PW-1A and PW-2

The inspectors reviewed records for the following welding activities:

SYSTEM WELD IDENTIFICATION WELD TYPE

Reactor Coolant Report # Work Order 339304-000, Tungsten Inert Gas

System ID # W-2 and W-3A, Safety relief Welding (GTAW)

valve drain line valve BBV0085

Reactor Coolant Report # Work Order 339304-005, Tungsten Inert Gas

System ID # W-2B and W-3, Safety relief Welding (GTAW)

valve drain line valve BBV0088

The inspectors verified, by review, that the welding procedure specifications and the

welder had been properly qualified in accordance with ASME Code,Section IX,

requirements. The inspectors also verified, through observation and record review, that

essential variables for the welding process were identified, recorded in the procedure

qualification record, and formed the bases for qualification of the welding procedure

specifications. Specific documents reviewed during this inspection are listed in the

attachment.

These actions constitute completion of the requirements for Section 02.01.

b. Findings

No findings were identified.

.2 Pressurized-Water Reactor Vessel Upper Head Penetration Inspection Activities

(71111.08-02.02)

a. Inspection Scope

During Wolf Creek Refueling Outage 19, a visual examination (VT-2) of the reactor

pressure vessel head was performed. The examination was in accordance with Code

Case N-729-1, Table 1, Item B4.20.

- 14 - Enclosure 2

Also, during the refueling outage, ultrasonic examinations of all seventy-eight control rod

drive mechanism penetration nozzles, and the eddy current examination of the vent line

in the reactor vessel head, was completed. No indications of primary water stress

corrosion cracking were identified. A number of thermal sleeves were found to have

wear extending up to as much as 360 degrees around the thermal sleeve where the

thermal sleeve exits the bottom end of the control rod drive mechanism head adapter

tube. Wear was found in rodded and unrodded penetration locations. The wear was

attributed by the licensee to the thermal sleeve contacting the inside diameter of the

control rod drive mechanism head adapter tube due to a flow-induced impact/whirling

motion of the thermal sleeve. The sleeve-to-adapter contact resulted in wear of material

on the outside diameter of the thermal sleeves.

The licensee informed the inspectors that no immediate remedial action was required.

The inspectors reviewed the licensees evaluation, analysis, and calculations and

concurred with their conclusions. The unrodded thermal sleeves in penetration locations

62 and 63 will need follow-up inspection and/or replacement. From the outer diameter

wear results, the sleeve in location 62 has a predicted life of three inspection cycles, and

the sleeve in location 63 has a predicted life of two inspection cycles. Therefore, the

licensee recommended that these two sleeves be inspected during future refueling

outages for emergent wear.

These actions constitute completion of the requirements for Section 02.02.

b. Findings

No findings were identified.

.3 Boric Acid Corrosion Control Inspection Activities (Pressurized-Water Reactors)

(71111.08-02.03)

a. Inspection Scope

The inspectors evaluated the implementation of the licensees boric acid corrosion

control program for monitoring degradation of those systems that could be adversely

affected by boric acid corrosion. The inspectors participated in containment walkdowns

for identifying locations of boric acid leakage, and reviewed the documentation

associated with the licensees boric acid corrosion control walkdowns as specified in

Procedures STN PE-040D and AI 16F-002. The inspectors also reviewed the visual

records of the components and equipment. The inspectors verified that the visual

inspections emphasized locations where boric acid leaks could cause degradation of

safety-significant components. The inspectors also verified that the engineering

evaluations for those components, where boric acid was identified, gave assurance that

the ASME Code wall thickness limits were properly maintained. The inspectors

confirmed that the corrective actions performed for evidence of boric acid leaks were

consistent with requirements of the ASME Code. Specific documents reviewed during

this inspection are listed in the attachment.

- 15 - Enclosure 2

These actions constitute completion of the requirements for Section 02.03.

b. Findings

.1 Failure to Follow Station Procedures.

Introduction. The inspectors identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to follow

procedures to accurately identify, characterize, and resolve boric acid leaks.

Specifically, the licensee failed to recognize discrepancies between boric acid control

procedures and failed to follow boric acid program procedures. Specifically, the licensee

failed to: (1) resolve discrepancies within the boric acid corrosion control program

procedure; (2) resolve discrepancies between the boric acid corrosion control program

procedure and the boric acid leak management procedure; and (3) failed to track and

resolve leakage for locations where health physics had installed drip catch

containments, to review the Health Physics Drip Bag Log as part of the quarterly outside

containment walkdown, and to add component locations to the program. Additionally,

the licensee failed to periodically assess the effectiveness of the program on a refueling

frequency.

Description. The inspectors reviewed station procedures AP 16F-001, Boric Acid

Corrosion Control Program, and AI 16F-002, Boric Acid Leakage Management. In

Procedure AP 16F-001, Attachment A, Section A.1, the least severe leakage where

dry boron residue is present is titled, Non-active Leak, and also classifies leaks into

four categories of severity (Non-Active, Small, Medium, and Large). In Section A.3,

however, the least severe leakage is titled, Inactive Leak. In Procedure AI 16F-002,

Attachment A.1, there are five levels of leakage severity (Non-active, Detectable, Small,

Medium, and Large). This procedure also directs screening/evaluation of boric acid

leakage deficiencies be completed per AI 16F-001, Evaluation of Boric Acid Leakage

(Steps 6.1.1.3, 6.1.2.3). However, the flowchart on Figure 1 references

screening/evaluation per AP 22A-001, Screening, Prioritization, and Pre-Approval,

Revision 15. The inspectors concluded that these procedures provided inconsistent

guidance that affected the licensees ability to properly classify and evaluate boric acid

leaks.

In Procedure AI 16F-002, Steps 5.2.5 and 6.1.5, require the program owner to track and

resolve leakage for locations where health physics had installed drip catch

containments, to review the Health Physics Drip Bag Log as part of the quarterly outside

containment walkdown, and to add component locations to the program. However, the

inspectors noted that consolidation of the health physics log into the Leak Management

program was not regularly completed or documented.

Additionally, steps 6.4.5 and 6.4.6 require the boric acid corrosion control program

owner to periodically assess the effectiveness of the program on a refueling frequency,

including actual performance versus program goals, recommendations for improvement,

summary of inspections/activities performed since last assessment, and a benchmarking

activity once per fuel cycle. However, the inspectors noted that self-assessments were

only completed for the quarterly outside containment walkdowns, and without

- 16 - Enclosure 2

identification of program goals. The inspectors concluded that the licensee was not

performing benchmarking and assessment activities as required by their Boric Acid

Corrosion Control Program.

The inspectors also noted a problem in the frequency of reevaluating past screenings.

Procedure AI 16F-002, Step 6.1.2.3.a. stated that screenings/evaluations for

components with current acid leakage/residue should be updated when the

screening/evaluation is more than 18 months old. However, the inspectors noted that

the station had current acid leakage/residue screenings/evaluations that had not been

updated after 18 months to assess if conditions were still bound by previous evaluations.

The inspectors noted that several condition reports indicated boric acid leakage

locations that had not been adequately identified or evaluated. Condition Report 38972,

initiated on May 9, 2011, indicated boron in the A spent fuel pool cooling pump room

sump. Multiple paths of in-leakage were listed as possible contributing causes to this

accumulation and the work request was closed without resolution of which path(s) were

leaking into the sump. The condition was considered expected and acceptable by

station personnel. Condition Report 60942 reported a large amount of boron build up

around the packing gland of spent fuel pool cleanup pump B, but noted that the same

condition was documented in previous Work Orders 12-356716-000 and Work

Request 12-095525. Condition Report 36024, initiated on March 29, 2011, reported a

leak in the refuel pool. The condition report listed the leak as low significance and not

expected to challenge the function of the refuel pool level limit. The refueling pool was

considered operable but degraded, and the condition report stated that leakage from the

refueling pool had been identified in the past, but the source of leakage was never

identified or evaluated.

The violation was entered into the licensees corrective action program as Condition

Report 65212.

Analysis. The inspectors determined that the failure to recognize discrepancies between

different boric acid control procedures, and the failure to follow boric acid program

procedures was a performance deficiency. The performance deficiency was more than

minor because it affected the Initiating Events Cornerstone attribute of procedure quality

and affected the cornerstone objective to limit the likelihood of those events that upset

plant stability and challenged critical safety functions during shutdown as well as power

operations, and if left uncorrected, the performance deficiency had the potential to lead

to a more significant safety concern. Specifically, failure to resolve discrepancies within

procedures or track and resolve leak locations where health physics had installed drip

catch containments had the potential to mischaracterize leaks or allow leaks to corrode

safety-related systems. Using Inspection Manual Chapter 0609, Appendix A, The

Significance Determination Process for Findings At-Power, the finding was determined

to be of very low safety significance (Green), because the finding was a procedure

quality problem that did not represent a loss of system safety function, and did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The finding had a cross-cutting aspect in the area of human

performance associated with the work practices component because the licensee failed

- 17 - Enclosure 2

to ensure supervisory and management oversight of work activities, including procedure

appropriateness and compliance, such that nuclear safety is supported H.4(c).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, states, in part, activities affecting quality shall be prescribed by

procedures of a type appropriate to the circumstance and accomplished in accordance

with these procedures. Contrary to the above, the licensee failed to prescribe activities

affecting quality by procedures of a type appropriate to the circumstance, and failed to

accomplish activities affecting quality in accordance with procedures. Specifically, the

licensee failed to recognize discrepancies between boric acid control procedures and

failed to follow boric acid program procedures Specifically, prior to February 19, 2013,

the licensee failed to: (1) resolve discrepancies within the boric acid corrosion control

program procedure; (2) resolve discrepancies between the boric acid corrosion control

program procedure and the boric acid leak management procedure; and (3) failed to

track and resolve leakage for locations where health physics had installed drip catch

containments, to review the Health Physics Drip Bag Log as part of the quarterly outside

containment walkdown, and to add component locations to the program. Further, the

licensee had failed to periodically assess the effectiveness of the program on a refueling

frequency. Because this finding was of very low safety significance, it was treated as a

Green non-cited violation in accordance with Section 2.3.2 of the NRC Enforcement

Policy. The violation was entered into the licensees corrective action program as

Condition Report 65212: NCV 05000482/2013003-01, Failure to Follow Station

Procedures.

.2 Failure to Identify Leakage at Refueling Pool Cavity.

Introduction. The inspectors identified Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for failure to assure that conditions

adverse to quality are promptly identified and corrected. Contrary to the above, the

licensee failed to identify and evaluate a condition adverse to quality in a timely manner.

Specifically, the licensee failed to document the large area of boric acid leakage and

corroded steel plates on the south primary shield wall of the containment refueling pool.

Description. During a boric acid walkdown on February 19, 2013, accompanied by the

licensees program owner, the NRC inspector noted a large area on the backside of the

refueling pool where residue existed around the perimeter of several steel plate

imbedments on two concrete walls and the ceiling that had not been previously identified

by the licensee. The residue had the appearance of a boric acid leak, and one of the

corners of the plates had noticeable corrosion. Procedure AP 16F-001, Boric Acid

Corrosion Control Program, Revision 6B, Step 6.2.1 stated, Sources of boron

seepage/leakage identified by plant personnel per 6.1.1 shall have the following actions

taken as applicable. The large area found on the exterior walls of the refuel cavity,

along with the corroded metal, were reasonable indications that a leak had been

occurring for a considerable amount of time, and should have been noted by station

personnel, as the area was easily accessible and traveled by personnel during refueling

outages. The licensee sent a sample of the residue off site to be analyzed. The results

of the sample identified the residue as boric acid. The licensee concluded that the boric

- 18 - Enclosure 2

acid residue was the result of leakage from the containment refueling pool with migration

through the primary shield wall concrete via construction joints and cracks.

This finding was entered into the licensees corrective action program as Condition

Report 64213.

Analysis. The inspectors determined that the failure to promptly identify and evaluate

the condition adverse to quality was a performance deficiency. The performance

deficiency was more than minor because it affected the Initiating Events Cornerstone

attribute of human performance and affected the cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations and, if left uncorrected, the performance

deficiency would have the potential to lead to a more significant safety concern.

Specifically, failure to implement corrective actions could result in increased leakage and

further degradation of the safety system. The finding has a cross-cutting aspect in the

area of human performance associated with the work practices component because the

licensee failed to define and effectively communicate expectations regarding procedural

compliance and that personnel follow procedures H.4(b).

Enforcement. The inspectors identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, which states, in part, Measures shall be

established to assure that conditions adverse to quality are promptly identified and

corrected. Contrary to the above, the licensee failed to assure that conditions adverse

to quality were promptly identified and corrected. Specifically, prior to February 19,

2013, the licensee failed to document the large area of boric acid leakage and corroded

steel plates on the south primary shield wall of the containment refuel pool. Because

this finding was of very low safety significance, it was treated as a Green noncited

violation in accordance with Section 2.3.2 of the NRC Enforcement Policy. This finding

was entered into the licensees corrective action program as Condition Report 64213:

NCV 05000482/2013003-02, Failure to Identify Leakage at Refuel Pool Cavity.

.3 Steam Generator Tube Inspection Activities (71111.08-02.04)

a. Inspection Scope

The inspectors reviewed the licensees in-situ pressure testing screening criteria for

flawed steam generator tubes to verify that it was in accordance with the EPRI

Guidelines. The inspectors also reviewed the steam generator tube eddy current

examination scope and expansion criteria to determine verify that these meet technical

specification requirements. Also reviewed was the licensees inspection of the

secondary side of the steam generators, and review of the licensees corrective action

taken in response to any observed degradation. The licensee did repairs on select

tubes (e.g., installed plugs or sleeves), and the inspectors observed a portion of these

repairs. The inspector observed the licensees vendor to determine if the equipment was

qualified for detection and/or sizing of the expected types of tube degradation. The

inspectors observed the licensees vendor performing analysis of the steam generator

tubes to determine if proper eddy current testing analysis techniques were applied.

- 19 - Enclosure 2

Wolf Creek is a four-loop plant with Model F steam generators. Each steam generator

includes nominally 5626 tubes made of Alloy 600 thermally treated (A600TI) material.

Wolf Creek had implemented an inspection plan in the past which had exceeded

industry inspection requirements. Prior to Refueling Outage 18, the inspection scope

was 100 percent in two steam generators each outage. The plan was changed to a

sampling inspection in all four steam generators each outage in accordance with the

results of the economic model (Letter SGMP-11-27, Justification of Change to

Inspection Plan for Wolf Creek, dated March 21, 2011).

The primary side inspection scope performed in all four steam generators for the current

outage (Refuel Outage 19) included the following:

  • 25 percent hot leg rotating pancake coil tube sheet +3"/-15.21"
  • Cold leg peripheral tubes, tube sheet cold +/- 3" 100 percent of peripheral tubes
  • +Point examination of all "1-code" indications that are not resolved after history

review

  • +Point inspection to bound (all surrounding tubes, at least 1 pitch removed) the

tubes with possible loose part signals during the current inspection

  • +Point inspection of possible loose part signals from the previous inspection as

specified in Section 3.5

  • 25 percent Row 1 and Row 2 U-bends, mid-range +Point examination
  • Dents (structures) >5 volts: Inspect 50 percent in steam generator band C, and

25 percent in steam generators A and D of all previously identified and all new

dents >5 volts in the hot leg (including the U-bends) with the mid-range +Point

probe in all four steam generators

  • Dings (free-span) >5 volts: Inspect 25 percent of all previously identified and all

new dings >5 volts in the hot leg (including the U-bends) with the mid-range

+Point probe in all four steam generators. A "new" ding is defined as one for

which there is no prior historical record

  • 100 percent bobbin inspection of all prior indications except dents and dings
  • +Point examination of a 5 percent sample of bobbin indications that have not

changed since the prior inspection ("H" and "S" codes)

  • +Point inspection of the sample of tubes to support the scale profiling effort

- 20 - Enclosure 2

  • I00 percent bobbin inspection of tubes identified as potentially having high

residual stress

  • 100 percent bobbin inspection of active tubes surrounding previously plugged

tubes

  • Visual inspections of all plugs, including factory installed plugs, or their

replacements

  • Inspection of potentially deleterious foreign objects (2 tubes)

During the inspection of the hot leg tube sheet expansion zone, a circumferential primary

water stress corrosion crack indication was detected in steam generator B. Due to this

indication, detected at row 17, column 89, tube sheet hot -6.26 inches, the hot leg

rotating pancake coil tube sheet inspection (+3" / -15.21") examination scope was

expanded to 100 percent of tubes in steam generator B with bulge or overexpansion

signals. In addition, the examination scope was confirmed to include at least 20 percent

of tubes in the three other steam generators with bulge or overexpansion signals. No

additional indications were detected. The maximum measured depth of the

circumferential primary water stress corrosion cracking indication in steam generator B

at row 17, column 89, was well below the condition monitoring limit; therefore, the

requirements for condition monitoring were satisfied. The tube was plugged and

because the indication is 6.26 inches inside the tube sheet, there is no concern with

lateral movement if the indication grows to result in tube severance. Because the tube is

unpressurized, there is no pull-out force to cause vertical motion. Therefore, there was

no need to stabilize the tube.

As a result of the eddy current inspection, sixteen tubes were plugged during Refueling

Outage 19. Five tubes in steam generator A, four tubes in steam generator B, two tubes

in steam generator C, and five tubes in steam generator D.

These actions constitute completion of the requirements for Section 02.04.

b. Findings

No findings were identified.

.4 Identification and Resolution of Problems (71111.08-02.05)

a. Inspection Scope

The inspectors reviewed 36 condition reports which dealt with inservice inspection

activities. For the majority of the condition reports, the corrective actions identified for

inservice inspection issues were appropriate. As noted in Section 1R08.3.b.2, the

licensee had missed some opportunities to comply with existing procedures in their

corrective action program. The issue identified in Section 1R08.3.b.2 was a condition

adverse to quality that the licensee failed to identify, therefore the concern of a boric acid

leak was never entered into their corrective action program.

- 21 - Enclosure 2

The inspectors had another observation of the licensees corrective action program,

where the licensee failed to properly evaluate industry generated operating experience.

In January 2012, the licensee received Westinghouse Nuclear Safety Advisory Letter 12-

1 (NSAL-12-1), pertaining to Steam Generator Channel Head Degradation. In January

2012, the licensee wrote Condition Report 00048149, referencing the information in the

Westinghouse Advisory Letter. Condition Report 00048149 stated that the information

is applicable to our steam generators; however, it is not an immediate concern. Wolf

Creek has been performing visual inspections of our steam generator channel heads for

many years. Most recently, the channel heads in all four steam generators were

inspected during RF18 with no anomalies identified. The licensee indicated that the

information would be incorporated as enhancements into work packages and

procedures. On February 22, 2013, during the current Refueling Outage RF19, a visual

inspection of steam generator A hot leg resulted in the licensee identifying a rust-colored

stain at the divider plate to channel head weld, towards the channel head side of the

weld. The stain was identified approximately six inches down from the tube sheet.

Following identification of the potential cladding degradation, ultrasonic testing was

attempted of the area from outside the steam generator primary bowl. The first attempt

was unsuccessful utilizing a straight beam ultrasonic testing probe due to interferences

with the steam generator support beam. Subsequently, a 60-degree L Wave ultrasonic

test probe was utilized to characterize the area. The results from the ultrasonic testing

identified the flaw to be approximately 0.1 inch deep by approximately 2 inches long.

No width could be obtained. The licensee classified the steam generator as degraded

but operable, and planned to perform further evaluation during the next scheduled

refueling outage.

Following the examination, the inspectors questioned the licensees results, conclusions,

and future plans. From this discussion, the inspectors identified that the licensee was

not in compliance with the American Society of Mechanical Engineers (ASME) Boiler

and Pressure Vessel Code. On February 28 and March 11, 2013, conference calls were

held with the NRC, the licensee, and Westinghouse, to discuss the issue of the rusted

area, the inspection techniques used to evaluate the flaw, and the licensees

conclusions. Following the initial conference call, the flaw at the edge of the divider

plate-to-channel head weld in steam generator A was evaluated by Wolf Creek Nuclear

Operating Corporation and Westinghouse, in accordance with Section XI, Paragraph

IWB-3510.1 and Table IWB-351 0-1, of the American Society of Mechanical Engineers

(ASME) Boiler and Pressure Vessel Code (ASME Code). The flaw was characterized as

a planar flaw. The licensee will perform a detailed fracture mechanics and fatigue

growth analysis of the flaw during the next operating cycle, in accordance with

Section XI of the ASME Code. The licensee will re-inspect this area during the next

refueling outage to determine the flaw growth rate.

The inspectors also questioned the licensee about historical documentation supporting

the licensees response that no anomalies had been identified during previous visual

inspections of the steam generators. The licensee performed a historical review of

visual inspections performed on steam generator A bowl that were on digital video discs

and noted that the rust spot was not visible in RF018, but was visible in RF017 and

- 22 - Enclosure 2

RF015. Steam generator A had not been inspected during RF016. Also, the rust spot

was visible in both the RF011 and RF07 video recordings. The RF07 (1994) video is the

earliest video recording of this area. The inspectors concluded that the licensee had

information available for review that should have been evaluated when responding to

Condition Report 00048149. The licensee had not utilized information identified in NRC

Inspection Manual Part 9900, Technical Guidance, such as examinations of records,

inservice testing and inspection programs, maintenance activities, operational event

reviews, operational experience reports, vendor reviews, or inspections, in their

response to Condition Report 00048149.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Quarterly Review of Licensed Operator Requalification Program

a. Inspection Scope

On June 11, 2013, the inspectors observed a crew of licensed operators in the plants

simulator during requalification training for steam generator tube rupture methodology

changes. The inspectors assessed the following areas:

  • Licensed operator performance
  • The ability of the licensee to administer the evaluations
  • The modeling and performance of the control room simulator
  • The quality of post-scenario critiques
  • Follow-up actions taken by the licensee for identified discrepancies

On June 11, 2013, the inspectors observed a crew of licensed operators in the plants

simulator during requalification training for inadvertent safety injection actuation. The

inspectors assessed the following areas:

  • Licensed operator performance
  • The ability of the licensee to administer the evaluations
  • The modeling and performance of the control room simulator
  • The quality of post-scenario critiques
  • Follow-up actions taken by the licensee for identified discrepancies

These activities constitute completion of two quarterly licensed operator requalification

program samples as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

- 23 - Enclosure 2

.2 Quarterly Observation of Licensed Operator Performance

a. Inspection Scope

On April 29, 2013, the inspectors observed the performance of on-shift licensed

operators in the plants main control room. At the time of the observations, the plant was

in a period of heightened activity due to a unit power reduction in support of emergent

work. The inspectors observed the operators performance of the following activities:

  • Primary reactivity changes: control rod manipulations and borations
  • Secondary load changes: automatic load set changes
  • Swap-over from main feed regulating valves to bypass feed regulating valves
  • Swap over of plant electrical loads from unit auxiliary transformer to the start-up

transformer

In addition, the inspectors assessed the operators adherence to plant procedures,

including AP 21-001, Conduct of Operations, and other operations department policies.

These activities constitute completion of one quarterly licensed-operator performance

sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

67570

  • Watertight pressure doors - Condition Report 65884
  • High energy line break doors - Condition Report 66874

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

- 24 - Enclosure 2

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance monitoring
  • Charging unavailability for performance monitoring
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of four quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

  • April 7, 2013, weekly risk assessment 13-202

- 25 - Enclosure 2

work

  • June 19, 2013, weekly risk assessment revision for Class 1E air conditioning unit

replacement

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four maintenance risk assessments

and emergent work control inspection samples as defined in Inspection

Procedure 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed the following assessments:

  • April 17, 2013, safety injection pumps A & B run with suction valves closed

and replacement

  • June 24, 2013, Class 1E air conditioning unit air flow calculation revision

The inspectors selected these operability and functionality assessments based on the

risk significance of the associated components and systems. The inspectors evaluated

the technical adequacy of the evaluations to ensure technical specification operability

was properly justified and to verify the subject component or system remained available

such that no unrecognized increase in risk occurred. The inspectors compared the

operability and design criteria in the appropriate sections of the technical specifications

and Updated Safety Analysis Report to the licensees evaluations to determine whether

- 26 - Enclosure 2

the components or systems were operable. Where compensatory measures were

required to maintain operability, the inspectors determined whether the measures in

place would function as intended and were properly controlled. Additionally, the

inspectors reviewed a sampling of corrective action documents to verify that the licensee

was identifying and correcting any deficiencies associated with operability evaluations.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three operability evaluations inspection samples

as defined in Inspection Procedure 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

.1 Permanent Modifications

a. Inspection Scope

The inspectors reviewed key affected parameters associated with energy needs,

materials, replacement components, timing, heat removal, control signals, equipment

protection from hazards, operations, flow paths, pressure boundary, ventilation

boundary, structural, process medium properties, licensing basis, and failure modes for

the permanent modifications listed below.

  • Installation of station blackout diesel generators

The inspectors verified that modification preparation, staging, and implementation did

not impair emergency/abnormal operating procedure actions, key safety functions, or

operator response to loss of key safety functions; post modification testing will maintain

the plant in a safe configuration during testing by verifying that unintended system

interactions will not occur; systems, structures and components performance

characteristics still meet the design basis; the modification design assumptions were

appropriate; the modification test acceptance criteria will be met; and licensee personnel

identified and implemented appropriate corrective actions associated with permanent

plant modifications. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of three samples for permanent plant

modifications, as defined in Inspection Procedure 71111.18-05.

b. Findings

No findings were identified.

- 27 - Enclosure 2

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

replacement

  • June 21, 2013, Class 1E air conditioning unit compressor replacement
  • June 22, 2013, spent fuel pool heat exchanger tube plugging

transmitter replacement

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

  • The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

  • Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated

Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of five post-maintenance testing inspection

samples as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings were identified.

- 28 - Enclosure 2

1R20 Refueling and Other Outage Activities (71111.20)

.1 Refueling Outage

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the refueling

outage already in progress at the beginning of this inspection period. Inspection

activities covered in this report were conducted March 1-April 16, 2013, to confirm that

licensee personnel had appropriately considered risk, industry experience, and previous

site-specific problems in developing and implementing a plan that assured maintenance

of defense in depth. During the refueling outage, the inspectors monitored licensee

controls over the outage activities listed below.

  • Configuration management, including maintenance of defense in depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service

  • Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing

  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error

  • Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities

  • Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system

alternative means for inventory addition, and controls to prevent inventory loss

  • Controls over activities that could affect reactivity

specifications

  • Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage

  • Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

- 29 - Enclosure 2

left which could block emergency core cooling system suction strainers, and

reactor physics testing

  • Licensee identification and resolution of problems related to refueling outage

activities

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and other outage

inspection sample as defined in Inspection Procedure 71111.20-05.

b. Findings

No findings were identified.

.2 Forced Outage

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the forced

outage to repair the Class 1E air conditioning unit A, conducted May 5-13, 2013, to

confirm that licensee personnel had appropriately considered risk, industry experience,

and previous site-specific problems in developing and implementing a plan that assured

maintenance of defense in depth. During the forced outage, the inspectors observed

portions of the shutdown and cooldown processes and monitored licensee controls over

the outage activities listed below.

  • Configuration management, including maintenance of defense in depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service

  • Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing

  • Licensee identification and resolution of problems related to forced outage

activities

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and other outage

inspection sample as defined in Inspection Procedure 71111.20-05.

b. Findings

No findings were identified.

- 30 - Enclosure 2

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Safety Analysis Report, procedure requirements,

and technical specifications to ensure that the surveillance activities listed below

demonstrated that the systems, structures, and/or components tested were capable of

performing their intended safety functions. The inspectors either witnessed or reviewed

test data to verify that the significant surveillance test attributes were adequate to

address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

  • Reference setting data

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

  • April 3, 2013, integrated diesel generator and safeguards actuation test train A

- 31 - Enclosure 2

  • April 4, 2013, integrated diesel generator and safeguards actuation test train B
  • April 24, 2013, manual start, synchronization, and loading of emergency diesel

generator A

(inservice test)

  • June 3, 2013, channel operational test of Tavg, T, and pressurizer pressure

protection set one

(inservice test)

valve test (inservice test)

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of seven surveillance testing inspection samples

as defined in Inspection Procedure 71111.22-05.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS2 Occupational ALARA Planning and Controls (71124.02)

a. Inspection Scope

This area was inspected to assess performance with respect to maintaining occupational

individual and collective radiation exposures as low as is reasonably achievable

(ALARA). The inspectors used the requirements in 10 CFR Part 20, the technical

specifications, and the licensees procedures required by technical specifications as

criteria for determining compliance. During the inspection, the inspectors interviewed

licensee personnel and reviewed the following items:

  • Site-specific ALARA procedures and collective exposure history, including the

current 3-year rolling average, site-specific trends in collective exposures, and

source-term measurements

  • ALARA work activity evaluations/post-job reviews, exposure estimates, and

exposure mitigation requirements

- 32 - Enclosure 2

  • The methodology for estimating work activity exposures, the intended dose

outcome, the accuracy of dose rate and man-hour estimates, and intended

versus actual work activity doses and the reasons for any inconsistencies

  • Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

  • Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

  • Audits, self-assessments, and corrective action documents related to ALARA

planning and controls since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.02-05.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment (71124.04)

a. Inspection Scope

This area was inspected to: (1) determine the accuracy and operability of personal

monitoring equipment; (2) determine the accuracy and effectiveness of the

licensees methods for determining total effective dose equivalent; and (3) ensure

occupational dose is appropriately monitored. The inspectors used the requirements in

10 CFR Part 20, the technical specifications, and the licensees procedures required by

technical specifications as criteria for determining compliance. During the inspection,

the inspectors interviewed licensee personnel, performed walkdowns of various portions

of the plant, and reviewed the following items:

  • External dosimetry accreditation, storage, issue, use, and processing of active

and passive dosimeters

  • The technical competency and adequacy of the licensees internal dosimetry

program

  • Adequacy of the dosimetry program for special dosimetry situations such as

declared pregnant workers, multiple dosimetry placement, and neutron dose

assessment

  • Audits, self-assessments, and corrective action documents related to dose

assessment since the last inspection

- 33 - Enclosure 2

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.04-05.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Security

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the

licensee for the first quarter 2013 performance indicators for any obvious inconsistencies

prior to its public release in accordance with Inspection Manual Chapter 0608,

Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific

activity performance indicator for the period from the second quarter 2012 through the

first quarter 2013. To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

The inspectors reviewed the licensees reactor coolant system chemistry samples,

technical specification requirements, issue reports, event reports, and NRC integrated

inspection reports for the period of April 2012 through March 2013 to validate the

accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified. In

addition to record reviews, the inspectors observed a chemistry technician obtain and

- 34 - Enclosure 2

analyze a reactor coolant system sample. Specific documents reviewed are described

in the attachment to this report.

These activities constitute completion of one reactor coolant system specific activity

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.3 Reactor Coolant System Leakage (BI02)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage

performance indicator for the period from the second quarter 2012 through the first

quarter 2013. To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

The inspectors reviewed the licensees operator logs, reactor coolant system leakage

tracking data, issue reports, event reports, and NRC integrated inspection reports for the

period of April 2012 through March 2013 to validate the accuracy of the submittals. The

inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one reactor coolant system leakage sample as

defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included the complete and accurate

identification of the problem; the timely correction, commensurate with the safety

significance; the evaluation and disposition of performance issues, generic implications,

- 35 - Enclosure 2

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective actions.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors focused their review on repetitive equipment

issues, but also considered the results of daily corrective action item screening

discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human

performance results. The inspectors nominally considered the 6-month period of

October 2012 through March 2013; although, some examples expanded beyond those

dates where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

- 36 - Enclosure 2

a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

These activities constitute completion of one single semi-annual trend inspection sample

as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

.4 Selected Issue Follow-up Inspection: Over-torquing Events

a. Inspection Scope

The inspectors recognized a potential trend in over-torquing events at Wolf Creek. The

inspectors observed two events: broken support screws on a Class 1E air conditioning

terminal box as well as over-torquing of the bonnet studs on a safety injection system

check valve. The inspectors reviewed the causes identified and actions taken for each

event. The inspectors also reviewed a previous finding written for over torque of the

essential service water strainer cover to stop leakage without consulting the design

bases of the materials and protective coatings. The inspectors performed a search of

the licensees corrective action database and identified three additional potential over-

torquing events within the last four years. The inspectors presented the events to the

licensee. The licensee wrote Condition Report 65799 to perform a basic trend analysis.

The inspectors reviewed the basic trend analysis.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

.5 Selected Issue Follow-up Inspection: Return to Full Qualification Fuel Cycle Carryover

a. Inspection Scope

During a review of items entered in the licensees corrective action program, the

inspectors recognized a corrective action item documenting the status of all open

operable/functional but degraded/non-conforming conditions that were being

re-evaluated at the end of the refueling outage to determine their suitability for deferral

through fuel cycle 20. All open degraded and non-conforming conditions must be re-

evaluated if they are not corrected during the next reasonable opportunity, such as a

refueling or mid-cycle outage, to ensure that the condition will meet all requirements for

safe operation until the next available opportunity to correct the condition.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

- 37 - Enclosure 2

b. Findings

No findings were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000482/2011-008-00: Post-Fire Safe Shutdown

Latent Design Issue May Cause Essential Service Water System Flow Imbalance

The inspector performed an in-office evaluation of circuit modification and engineering

change package documentation.

On July 20, 2011, during a review of the post fire safe shutdown analysis for

valve EFHV0060, ESW Return from Component Cooling Water Heat Exchanger, the

licensee identified a condition where a fire in the control room could cause the valve to

open and could be damaged such that the valve could not be manually closed. The

direct cause was a latent design deficiency that did not ensure that the valve was

isolated and protected from the potential effects of a control room fire. The licensee

verified that an hourly fire watch was in place in the control room and ensured the fire

watch would remain in place until the issue was resolved.

The licensee generated Engineering Change Package 013898 to modify the control

circuit for the valve. This modification rewired the torque and limit switches to ensure

they are not bypassed by a potential control room hot short (Information Notice 92-18

concern) and installed an isolation/close switch, EFHS0060, to isolate the control room

portion of the circuitry and also to close the valve.

The inspector reviewed the control circuitry modification and engineering change

package, and had discussions with the licensee concerning procedure changes that are

needed as a result of the modification. The inspector verified that the torque and limit

switches would not be bypassed by a hot short in the control room portions of the circuit.

The inspector verified that the isolation/close switch effectively isolated the control room

portions of the circuit and inserted redundant fuses into the control circuit for the valve.

No findings were identified and no violation of NRC requirements occurred. This LER is

closed.

.2 (Closed) Licensee Event Report 2013-003-00: Movement of Irradiated Fuel Progressed

After Non-Conservative Decision Making Resulted in Removal of One Source Range

Monitor from Service

The licensee reported that fuel movement was delayed past the scheduled completion

time due to an equipment problem. Scheduled work on a source range nuclear

instrument was begun while still in the refueling operating mode, when both source

range monitors were required to be operable. The inspectors screened this event using

Inspection Manual Chapter 0612 Appendix B and determined that the performance

deficiencies involved were minor,. Because no fuel movement or other reactivity

- 38 - Enclosure 2

manipulations were in progress during the time this instrument was inoperable. No

additional issues were identified. This LER is closed.

.3 (Closed) Licensee Event Report 2013-005-00: Fatigue Failure of Jacket Water Pressure

Switch Diaphragm Results in Loss of the B Diesel Generator

a. Inspection Scope

The licensee reported that on March 13, 2013, emergency diesel generator B was

rendered inoperable by an equipment failure while emergency diesel generator A was

out of service for planned maintenance during a refueling outage. The licensee declared

a Notice of Unusual Event in accordance with station procedures until emergency diesel

generator B was repaired. The inspectors reviewed the event and the cause evaluation

and determined that this event did involve a violation of regulatory requirements. This

licensee event report is closed.

b. Findings

Diesel Generator Pressure Switch Failed Due to Instrument Line Pressure Oscillations

Introduction. A self-revealing, Green non-cited violation of 10 CFR Part 50. Appendix B,

Criterion XVI, Corrective Action, was identified on March 13, 2013. Specifically, the

licensee repeatedly replaced a jacket water pressure transmitter, but failed to correct

pressure oscillations that caused a fatigue failure of a pressure switch diaphragm, which

rendered emergency diesel generator B inoperable.

Description. On March 13, 2013, the reactor was defueled for a planned refueling

outage and the A emergency diesel generator disassembled for planned maintenance.

At 1:34 a.m. the control room received the B diesel generator trouble alarm. The local

operator found the shutdown relay in the control cabinet had actuated and would not

reset. The engine was declared inoperable and Wolf Creek declared a Notice of

Unusual Event for having two onsite electrical sources unavailable. Instrumentation and

controls technicians troubleshooting the condition determined that the control circuitry

was working properly, but a jacket water pressure switch diaphragm had failed and the

water that leaked was shorting and grounding the associated electrical switch, causing a

false positive signal. This pressure switch was used to indicate that the engine was

running, because the system pressure would be generated by an engine-driven pump.

This false signal rendered the engine inoperable because the resulting logic state

indicated the engine was running with no lube oil pressure, which locked in a protective

engine trip, preventing the engine from starting. The pressure switch was repaired and

the engine was tested and returned to service on March 14, 2013, at 2:21 a.m.,

terminating the Notice of Unusual Event. The licensee wrote Condition Report 65624 to

correct and identify the cause of this condition. This condition only affects the engine

while in standby; if the engine is operating the system would continue to run.

A hardware failure analysis performed on the diaphragm identified that the failure

mechanism was low stress, high cycle fatigue. The pressure switch was nearing the end

- 39 - Enclosure 2

of its specified lifetime; however, there was also a specification for the switch not to

exceed 33,000 pressure cycles to avoid diaphragm failure. The licensee was only

counting the diesel generator stops and starts as a single pressure cycle. However a

review of the machinery history found that a known equipment condition of the jacket

water pressure transmitter hunting had been observed since 2002. This condition was

inducing pressure oscillations in the shared instrument line every one or two seconds

when the engine was running. Furthermore, the magnitude of the oscillations grew as

the pressure transmitter hunting conditions worsened over time. The inspectors

concluded that the licensee focused on correcting the apparent source of the pressure

oscillations, but failed to evaluate the effects of the pressure cycles on components

exposed to the same oscillations. The inspectors noted that the transmitter had been

replaced 10 times between 2002 and 2012. Since the replacements also eventually

exhibited this behavior, the licensee recently determined that is indicative of an

underlying design issue, in that the transmitter model was not being used in the intended

application. Wolf Creek was planning a system modification address and permanently

correct this concern long term, but will be controlled through preventive maintenance in

the interim. Wolf Creek also added preventive maintenance activities to monitor the

replacement diaphragm and other interfacing components.

This issue was entered into the licensees corrective action program as Condition

Report 65624

The inspectors noted that having both emergency diesel generators inoperable at the

same time was permitted by technical specifications at the time of the failure, since the

reactor was defueled. Therefore, no required safety function was lost. The inspectors

also noted that declaration of a Notice of Unusual Event was inconsistent with having no

technical specification requirement to have the function available. Further review noted

that Wolf Creek had not adopted industry standard emergency action level guidance,

which would not have required an event declaration in these circumstances. The

licensee stated that they planned to evaluate adopting the latest guidance.

Analysis. Failure to analyze the effects of pressure oscillations in the emergency diesel

jacket water system on interfacing system components is a performance deficiency. The

performance deficiency is more than minor because it affected the equipment

performance attribute of the Mitigating Systems cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Inspection Manual Chapter 0609 Appendix A,

Significance Determination Process for Findings At Power, and determined that the

finding screens as very low safety significance (Green) because the finding does not

meet any criteria outlined in the Exhibit 2, Section A. Specifically, the finding is not a

loss of system safety function and did not exceed its technical specification allowed

outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The inspectors determined that the finding had a cross-cutting

aspect in the area of problem identification and resolution evaluations because the

licensee failed to ensure that issues that potentially affect nuclear safety are fully

evaluated and addressed in a timely manner. In particular, the licensee repeatedly

replaced the pressure transmitter ten times between 2002 and 2013, including five times

in 2011 and 2012, but failed to evaluate the effect of the pressure oscillations on an

affected component with a limited fatigue life P.1(c).

- 40 - Enclosure 2

Enforcement. Title 10 CFR Part 50. Appendix B, Criterion XVI, Corrective Action,

requires, in part, that Measures shall be established to assure that conditions adverse

to quality are promptly identified and corrected. Contrary to the above, between January

26, 2001, and March 13, 2013, the licensee failed to correct a condition adverse to

quality affecting the jacket water system associated with emergency diesel generator B.

Specifically, despite repeatedly replacing the pressure transmitter that was believed to

be the source of the pressure oscillation, the licensee failed to correct the condition, and

as a result, failed to prevent the subsequent fatigue failure of a pressure switch

diaphragm that rendered the system inoperable. Because the finding is of very low

safety significance and was entered into the licensees corrective action program as

Condition Report 65624, the violation will be treated as a non-cited violation in

accordance with Section 2.3.2.a of the NRC enforcement policy.

NCV 05000482/2013003-03, Diesel Generator Pressure Switch Failed Due to

Instrument Line Pressure Oscillations.

.4 Notice of Unusual Event for a Fire Lasting Greater than 15 Minutes on the Auxiliary

Boiler Roof

a. Inspection Scope

At 2:55 p.m. on April 11, 2013, the fire brigade was called to muster in response to a

confirmed fire in the southeast corner stairway of the turbine building. The inspectors

responded to the control room and to the scene of the fire. The fire was put out, but the

fire re-flashed underneath the insulation. Operations personnel secured the auxiliary

boiler, and the brigade moved onto the turbine building roof where the source of the

stairwell fire was identified as the exhaust stack penetration. Suppression was again

used, but thermal imaging cameras continued to identify hot spots as the fire re-flashed

beneath the stack insulation. Offsite local fire departments responded to the site to

assist with and disassembly and suppression activities until 4:48 p.m., when the fire was

confirmed to be out.

The cause of the fire was believed to an improper repair to the building roof. When the

roof was resealed, the roofers were unable to remove all of the tar and roofing materials

around the penetration, and they insulated over it. After approximately 2 months of

prolonged auxiliary boiler operation during the spring refueling outage, enough heat had

conducted through the stack to ignite the roofing debris. The exhaust stack penetration

has since been repaired. The inspectors screened this event using Inspection Manual

Chapter 0612 Appendix B and determined that the performance deficiencies involved

were not more than minor. All reporting requirements of 10 CFR 50.72 were met. The

inspectors assessed this fire brigade response to satisfy the annual brigade sample in

Section 1R05.

b. Findings

No findings of significance were identified.

- 41 - Enclosure 2

.5 Unplanned Positive Reactivity Transient While Swapping Turbine Operating Modes

a. Inspection Scope

The inspectors reviewed the sequence of events associated with an unplanned power

increase that occurred at 9:35 p.m. on May 2, 2013. Control room operators were

increasing power coming out a forced outage to repair a stator cooling water leak. With

the reactor holding at 79 percent power, operators planned to swap the turbine from full

arc steam admission mode (all four steam control valves throttling equally), the mode

used for turbine startup, and into the partial arc mode (three control valves fully open,

one throttling partially closed) used at full power. During the mode swap, the plant

experienced an unexpected power increase of 11 percent.

The inspectors reviewed procedures for reactivity management and reactivity

manipulations, as well as operator statements. The inspectors reviewed the cause of

the event and corrective actions taken. The inspectors reviewed a recent digital

instrumentation and controls modification to the turbine control system implemented in

the spring 2013 refueling outage.

b. Findings

.1 Failure to Update Station Procedures and Train Operators Regarding the Effects of

Design Changes to the Main Turbine Control System

Introduction. A Green self-revealing non-cited violation of Technical Specification 5.4.1a

was identified for the failure to properly update operating procedures and train operators

on the effects of a recently installed modification. Specifically, procedures were not

adequately revised to provide guidance for operating the new Westinghouse Ovation

digital turbine control system. As a result, operators shifted operating modes at a power

level that caused an unexpected 11 percent power increase due to the combined

characteristics of the steam control valves and the turbine control system. Additionally,

operators received training on shifting control modes at low power, where minor

transients occurred, but were not restricted from performing the swap at high power

levels where the transient could be more significant.

Description. The main turbine controls had been replaced in March 2013 as part of a

planned upgrade during a refueling outage. The controls had satisfactorily passed post

maintenance testing under Temporary Procedure TMP 12-016 during the refueling

outage restart two weeks earlier. During the first plant startup after the modification,

operators initiated the control mode swap below 50 percent reactor power. However, on

May 2, 2013, following an unplanned outage, the turbine control mode swap was

initiated at 76 percent power. As a result, reactor power increased 11 percent power

increase from 76 to 87 percent over a period of 5 minutes.

The following morning the licensee contacted the engineers who had prepared the

modification as well as the vendor (Westinghouse Ovation). The licensee learned that

such a transient was not unexpected under open loop controlling conditions; however,

swapping from full to partial arc mode in that condition is not recommended and should

- 42 - Enclosure 2

be avoided by procedure. Performing the full to partial arc swap in the megawatts

electric or steam pressure control modes will not result in a more than minimal

(1-2 percent) power transient because there is feedback in the circuit to limit changes in

turbine load.

The licensee determined that the mode swap was done in the open loop such that the

controller was programmed with the turbine control valve throttling characteristics as a

substitute for a system response feedback loop. The licensee confirmed earlier testing

that showed the valve characteristics were reasonably accurate below 50 percent power,

but were less accurate at higher powers. Since the turbine controller simultaneously

changed the position of all control valves, three valves were opening while the fourth

valve was to throttle down to compensate for the other three valves. The licensee had

demonstrated that the power transient during mode swap below 50 percent power

stayed within +/-3 percent of the initial power level, and returned to the original power

level. However, starting at 76 percent power, the mode swap resulted in a prolonged

power increase.

The inspectors reviewed the procedures and found that Procedure TMP 12-016

Post Modification Main Turbine Control System Generator Startup and Testing,

Revision 7, used for the post installation testing had steps to take the turbine controller

out of open loop mode before swapping from full to partial arc or vice versa. There was

no caution or warning in the procedure not to perform the swap in open loop mode.

However, there was no step, precaution, limitation, or warning in system operating

Procedure STS AC-001, Main Turbine Valve Testing, Revision 7, to remove the

controller from open loop prior to swapping modes. Control room operators were not

familiar with this potential risk from training either.

The inspectors noted that operator training on the new turbine controller had been

conducted below 50 percent power only. Prior to the modification in the spring 2013

refueling outage, the old turbine control system did not allow open loop control to be

selected. The inspectors determined that this was a new failure mechanism or

vulnerability introduced by the modification and should have been identified in the

planning stages and specifically addressed in the close out process specified in

Section 6.3.4 of AP 05-005, Design, Implementation & Configuration Control of

Modifications, by adding appropriate steps and cautions to procedure SYS AC-001.

This issue was entered into the licensees corrective action program as Condition

Report 68711.

Analysis. Failure to update station operating procedures to provide adequate guidance

for design changes to the turbine control system, and failure to adequately train

operators on those design changes, is a performance deficiency. The performance

deficiency is more than minor because it affected the design control, procedure quality,

and human performance attributes of the Initiating Events cornerstone objective to limit

the likelihood of events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. Using Inspection Manual Chapter 0609

Appendix A, Checklist 1, Initiating Events Screening Questions, the inspectors

determined that the finding was of very low safety significance (Green) because the

- 43 - Enclosure 2

finding did not result in a reactor trip coincident with the loss of mitigation equipment.

The inspectors determined that this finding had a cross-cutting aspect in the area of

human performance area of work control because the licensee did not appropriately

communicate and coordinate during activities in which interdepartmental coordination

was necessary to assure plant and human performance. Specifically, Wolf Creek did not

communicate and coordinate to ensure that procedure guidance and operator training

adequately conveyed the operational impacts and limitations associated with shifting

turbine control modes at different power levels H.3(b).

Enforcement. Technical Specification 5.4.1a requires that programs specified in the

Appendix A to Regulatory Guide 1.33, Revision 2, be established, implemented, and

maintained. Regulatory Guide 1.33, Appendix A, Section 2.f, includes a general plant

operating procedure for changing load and load following. Contrary to the above, from

April 13 to May 2, 2013, the licensee failed to maintain a general plant operating

procedure for changing load. Specifically, procedure GEN-00-004, Power Operations,

Revision 69, were not updated to provide adequate guidance swapping turbine steam

admission configurations following installation of a new turbine control system. Because

this finding is of very low safety significance and was entered into the licensees

corrective action program as Condition Report 68711, it is being treated as a non-cited

violation in accordance with section 2.3.2.a of the NRC Enforcement Policy:

NCV 05000482/2013003-04, Failure to Update Station Procedures and Train Operators

Regarding the Effects of Implemented Design Changes to the Main Turbine Control

System.

.2 Failure to Properly Manage Reactivity Changes when Swapping Turbine Steam

Admission Modes from Full to Partial Arc

Introduction. Inspectors identified a Green non-cited violation of Technical

Specification 5.4.1.a. for the failure to follow Conduct of Operations and Reactivity

Management procedures.

Description. The inspectors responded to an unplanned reactor transient that occurred

on the night of May 2, 2013. The licensee was increasing power from an unplanned

outage to repair a stator cooling water leak. The unexpected power increase occurred

while swapping the mode of turbine from full to partial arc steam admission while

controlling in the open loop (valve position) mode. This mode swap changes the turbine

control valves that throttle steam to go from all four valves equally throttling to three

valves fully open and one valve throttling such that all four valve slowly reposition over a

period of about 2.5 minutes. The main turbine controls had been replaced in March as

part of a planned upgrade during a refueling outage.

During the first plant startup after the modification, operators initiated the control mode

swap below 50 percent reactor power. However, on May 2, 2013, the mode swap was

initiated at 76 percent power. During the 2.5 minute swap, reactor power increased

11 percent power increase from 76 to 87 percent over a period of about 5 minutes. The

power increase caused Tavg to be below the programmed value for Tref, so the control

rods stepped out until fully withdrawn. The power increase continued, resulting in a

- 44 - Enclosure 2

7 degree Tavg-Tref mismatch as the secondary power demand overcooled the reactor.

Primary pressure lowered by 14 psi, and came within 1 psi of the Departure from

Nucleate Boiling technical specification limit of 2220 psi.

The inspectors reviewed plant parameter graphs during the period of the transient as

well as statements by operators and nuclear engineers in the control room at the time of

the transient. The inspectors concluded that operators had conducted a pre-job brief,

but had failed to discuss the expected plant response in detail, and failed to discuss

contingency actions if the plant response was not as expected. During the transient,

operators discussed taking action to terminate the transient, but were unable to

determine if there was a way to stop the valve swap once it started. Instead, they

attempted to verify that plant parameters did not exceed limits as the transient took its

full course.

The inspectors noted that the pre-job brief and operator response was contrary to the

reactivity control program. Specifically, operators failed to define the expected plant

response and have contingency actions ready in case the plant response was not as

expected. Operation of the main turbine controls was a reactivity manipulation as

defined in Procedure AP 19E-002, Reactivity Management Program, Revision 16.

Following the transient, the inspectors determined that the operators did not adequately

investigate the cause of the unexpected system response before continuing with the

power increase. The inspectors determined that the shift staffing that night did not

include a system expert or vendor representative for the new digital turbine controls to

help investigate the system response. After consulting with the reactor engineers and

the Operations Manager, operators concluded that the turbine controls were behaving as

expected and they had proper control, with the exception of the full to partial arc swap.

The inspectors determined that although the hypothesis was later proven to be correct,

they did not have adequate technical basis to show that equipment that impacts

reactivity was not malfunctioning. No functionality assessment or troubleshooting was

performed, and no technical experts were consulted to verify that the turbine control

response was understood before making the decision to raise power to 100 percent.

The licensee did not gain a full understanding of the event until their discussions with

engineers and the vendor (Westinghouse Ovation) the following morning. Wolf Creek

was informed that such a transient was not unexpected under open loop controlling

conditions, and should have been procedurally prohibited. The licensee was able to

replicate the system response in the plant simulator, both below 50 percent and at

76 percent power. The licensee therefore concluded that the system response was not

anomalous, and that continued operation was appropriate.

AP 19E-002 Reactivity Management Program Section 6.1.1 details the program:

The Reactivity Management Program is the systematic and philosophical direction given

to controlling evolutions with the potential to affect the reactivity and/or integrity of

nuclear fuel. This systematic process ensures that:

- 45 - Enclosure 2

  • All deliberate reactivity changes are planned and conducted in a controlled

conservative manner

  • Unexpected reactivity changes are minimized
  • Conservative actions are taken in response to unexpected reactivity changes
  • Reactivity-related modifications, analyses, predictions, and procedures are

correct and effectively implemented

Procedure AP 19E-002 Reactivity Management Program section 5.6 specified that

licensed operator responsibilities as follows:

Licensed Operators are responsible for the implementation of the Reactivity

Management Program. They are responsible for control of reactivity and taking

conservative actions to safeguard the integrity of the reactor fuel. Licensed operators

have the authority to terminate any activity in which the effects on reactivity control are

unknown, unexpected, or non-conservative.

Procedure AP 21-001, Conduct of Operations, also provides guidance on reactivity

management:

  • Section 6.1.1.1 states, The greatest responsibility of all licensed operators is to

ensure the reactivity condition of the reactor is monitored and conservatively

controlled at all times.

  • Section 6.1.3.1 notes In cases of unplanned reactivity evolutions, licensed

operators must promptly take actions to keep power below 100 percent, stop,

evaluate the plant conditions and take the appropriate conservative action.

Licensed operators shall not hesitate to reduce power, stabilize the plant, or trip

the reactor as necessary to protect the reactor core with concurrence from the

Control Room Supervisor.

Appendix A of this procedure specifies the content of reactivity briefs. The guidance

requires a detailed estimated start and stop point for reactor power as well as an

expected rate of change. Furthermore, contingency actions are to be determined

beforehand if these expectations are not met.

Operator statements and interviews indicate that the anticipated transient was about

1.5 percent, not to exceed 2 percent of rated electric and thermal power. No

contingency actions were specified during the brief. The inspectors determined that the

lack of this contingency planning contributed to the magnitude of the transient and lack

of operator response. For example, by not establishing a limit on the expected plant

response (e.g., require action if power increased above the expected 2 percent rise, or

failed to return to the starting power level) operators were unsure whether action was

needed, and defaulted to the generic Technical Specification limits. As a result, they

failed to act, even when the Tavg-Tref mismatch exceeded operational limits, the

- 46 - Enclosure 2

departure from nucleate boiling pressure limit was closely approached, and control rods

were unable to further compensate. The inspectors noted that later guidance from the

vendor established that operators could have terminated the power excursion at any

time simply by returning turbine steam controller to full arc mode, and thus restoring the

hold previously in place.

The inspectors also concluded that the licensees post-job review of transient lacked the

specific information needed to determine whether the turbine control system had

behaved as expected or had malfunctioned prior to deciding to proceed with power

ascension. In both the pre- and post-job cases, a lack of technical understanding about

the proper workings of the turbine controls was not recognized, and although not

deliberately, operators did proceed in the face of uncertainty. This issue was entered

into the licensees corrective action program as Condition Report 68711.

This issue was entered into the licensees corrective action program as Condition

Report 68711.

Analysis. Failure to provide contingency actions for a greater than anticipated reactor

transient in the pre-job reactivity brief is a performance deficiency. The performance

deficiency is more than minor because it affected the human performance attribute of the

Initiating Events cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. The inspectors evaluated the finding using Inspection Manual Chapter 0609

Appendix A, Checklist 1, Initiating Events Screening Questions, and determined that

the finding was of very low safety significance (Green) because the finding did not result

in a reactor trip coincident with the loss of mitigation equipment. The inspectors

determined that this finding had a cross-cutting aspect in the human performance area

of work practices because the licensee failed to communicate human error prevention

techniques, such as holding pre-job briefings, self and peer checking commensurate

with the risk of the assigned task, such that work activities were performed safely, and

personnel do not proceed in the face of uncertainty or unexpected circumstances.

Specifically, control room operators pre-job reactivity brief was not commensurate with

the risk of the assigned task, and station personnel proceeded to further raise power in

the face of uncertainty about the functionality of the turbine control system H.4(a).

Enforcement. Technical Specification 5.4.1.a requires that programs specified in

Appendix A to Regulatory Guide 1.33, Revision 2, be established, implemented, and

maintained. Regulatory Guide 1.33, Appendix A, Section 1.b includes administrative

procedures covering authorities and responsibilities for safe operation and shutdown.

Contrary to the above on May 2, 2013, did not fully implement the authorities and

responsibilities for safe operation and shutdown. Specifically, operators failed to follow

the Procedure AP 21-001, Conduct of Operations, Revision 61, Appendix Section 1.a.

requirement to establish contingency actions in advance to a planned reactivity

manipulation, in the event that the reactivity addition should exceed the planned amount.

Because this finding is of very low safety significance and was entered into the

licensees corrective action program as Condition Report 68711, it is being treated at a

non-cited violation in accordance with section 2.3.2.a of the NRC Enforcement Policy:

- 47 - Enclosure 2

NCV 05000482/2013003-05, Failure to Properly Manage Reactivity Changes when

Swapping Turbine Steam Admission Modes from Full to Partial Arc.

.6 Unplanned Shutdown due to Non-Functional Class 1E Air Conditioning Unit

On the evening of May 6, 2013, Wolf Creek station operators observed an increasing

trend in the temperature of the train A Class 1E AC and DC switchgear rooms.

Troubleshooting identified that a blockage was present in the thermal expansion valves

that was restricting refrigerant flow. The air conditioning unit itself was declared non-

functional. For systems needed to support the Class 1E AC and DC sources,

Wolf Creek was required to enter the applicable multiple technical specifications. Having

two inverters inoperable was not covered by a specific action statement, so the licensee

appropriately entered Technical Specification 3.0.3, and the unit was shut down to

Mode 5 so that the refrigerant system could be cleaned. Wolf Creek also used this

outage to replace the compressor in this air conditioning unit and chemically clean the

refrigerant system. No findings were identified.

.7 (Open) Notice of Enforcement Discretion (NOED) 13-4-002 for a Non-Functional Class

1E Air Conditioning Unit

On June 17, 2013, an oil sample taken from the train A Class 1E air conditioning unit

was found to have unacceptable levels of aluminum particulate, indicating that internal

parts were degrading and long term reliability was not assured. The unit was declared

non-functional and Wolf Creek again entered Technical Specification 3.0.3 at 11:11 a.m.

Wolf Creek requested a NOED that was granted by the NRC staff at 4:07 p.m. The

inspectors reviewed the documentation, plant status information, the equipment history,

as well as the Inspection Manual Chapter 0410 process. Consistent with NRC policy,

the NRC agreed not to enforce compliance with the specific technical specifications in

this instance, but will further review the cause(s) that created the apparent need for

enforcement discretion to determine whether a violation of NRC requirements existed.

This will be tracked under unresolved item (URI)05000482/2013003-06,

NOED 13-4-002 for a Non-functional Class 1E Air Conditioning Unit.

.8 (Closed) Licensee Event Report 2009-005-01, Loss of Both Diesel Generators with All

Fuel in the Spent Fuel Pool

The inspectors reviewed this LER and determined that the changes to the cause had

already been presented to and inspected by the 95001 inspection team. The results of

this inspection can be found in inspection report 05000482/20130 (ADAMS Accession

Number ML13126A197). LER 2009-005-01 is closed.

4OA5 Other Activities

Falsification of Spent Fuel Pool Area Housekeeping Inspection Records

a. Inspection Scope

The inspectors reviewed procedures and records associated with the conduct and

- 48 - Enclosure 2

completion for housekeeping inspections and foreign material exclusion from important

systems. The inspectors interviewed licensee staff, reviewed inspection records, station

procedures and security card reader logs.

b. Findings

Introduction. The inspectors identified a Severity Level IV violation of 10 CFR 50.9,

Completeness and Accuracy of Information, for the failure to maintain complete and

accurate records required by a license condition. Specifically, the licensee failed to

maintain complete and accurate records of the spent fuel pool area housekeeping

inspections for the period of October through December 2008, required by License

Condition 2.C.5, Fire Protection.

Description. On January 17, 2009, inspectors identified a non-cited violation of Technical

Specification 5.4.1.a, Procedures, for the failure to follow Procedure AP 12-003, Foreign

Material Exclusion, during a walkdown of the spent fuel pool area. During this walkdown,

the inspectors identified numerous untracked tools, equipment and duct tape attached to

various tools such that duct tape was located above and below the fuel pool water level.

In response to the violation, licensee Quality Assurance personnel conducted a review of

the problem that led to the NRC violation. During the review it was identified that the

housekeeping inspection reports had not identified the condition in the spent fuel pool

area. The licensee reviewed the fuel building card reader logs and determined that the

individual assigned to perform the housekeeping inspection in the spent fuel pool area had

not entered the area for a period of 3 months. The licensee determined that the individual

(a supervisor) had reported the information based on feedback received from others who

performed the actual housekeeping observation. Revision 6C of the procedure allowed for

a designee to perform the inspection instead of the management assigned individual. The

ability to designate another individual to perform the inspection was removed when the

procedure was updated in Revision 7 on November 10, 2008, and therefore not allowed

when the December 2008 inspection was completed. In response, the licensee revised

the procedure again to allow for a qualified designee to perform the inspections in

Revision 8, which was issued on September 17, 2009.

NRC inspectors identified that the individual questioned workers who had been in the area

about the condition of the housekeeping before signing off on the inspection with no

issues during the months of October and November 2008. The individual rationalized that

he had met the intent of the inspection, but failed to ask specific questions to ensure that

the inspection met the criteria stated in Attachment B, Building/Area Inspection Checklist.

The inspectors also determined that the individuals had not been designated to perform

the housekeeping inspection, or even told why they were being asked about the condition

of the area. Additionally, the inspectors identified that only one of the people that the

individual had questioned had actually entered the spent fuel pool area in the month of

October 2008. The person that the individual identified as having been questioning to

determine the status of the spent fuel pool area in November 2008, did not access the

spent fuel pool area that month. On December 4, 2008, the individual documented the

completion of an inspection with no issues in the Housekeeping Inspection Card without

- 49 - Enclosure 2

questioning any individuals or entering the area. The individual stated he knew work had

not been performed in the area since the previous report on November 25, 2008, so he

assumed that the condition remained unchanged.

The NRC determined that from October through December 2008, a licensee employee

failed to perform inspections of the spent fuel pool area in accordance with Procedure

AP 12-001, Housekeeping Control, and willfully documented false information on the

Housekeeping Inspection Cards.

The falsified inspection report was related to a housekeeping inspection procedure that

implements housekeeping inspections required by the fire protection program. The Wolf

Creek Updated Final Safety Analysis Report describes the fire protection program in

Section 9.5-1, and commits to meeting Regulatory Guide 1.39, Housekeeping

Requirements for Water-Cooled Nuclear Power Plants, Revision 2, Appendix 3A,

Conformance to NRC Regulatory Guides. Regulatory Guide 1.39, Revision 2, endorses

ANSI Standard N45.2.3-1973, Housekeeping During the Construction Phase of Nuclear

Power Plants, as a method of complying with fire protection program housekeeping

requirements. The ANSI Standard requires that periodic inspection and examination of

the work areas shall be performed at scheduled intervals to assure adequacy of

cleanliness and housekeeping practices, and that copies of inspection and examination

records shall be prepared and placed with other project records.

Analysis. The failure to maintain records required by License Condition that are complete

and accurate in all material respects in accordance with 10 CFR 50.9 was a violation.

Because the violation is associated with willfulness and impacted the regulatory process it

was evaluated under the traditional enforcement process as set forth in the NRC

Enforcement Policy. Since this violation was the result of a willful action, the NRC

considers the violation to be more than minor, and therefore, the NRC has classified the

violation at Severity Level IV, in accordance with the NRC Enforcement Policy (Section

4OA5).

Enforcement. Title 10 CFR 50.9 requires, in part, that information required by statute,

orders, or license conditions to be maintained by the licensee shall be complete and

accurate in all material respects.

Wolf Creek License Condition 2.C.5, Fire Protection, requires that the licensee shall

implement and maintain in effect all provisions of the approved fire protection program as

described in the SNUPPS Final Safety Analysis Report. The Wolf Creek Updated Final

Safety Analysis Report describes the fire protection program in Section 9.5-1, and

commits to meeting Regulatory Guide 1.39, Housekeeping Requirements for Water-

Cooled Nuclear Power Plants, Revision 2, in Appendix 3A, Conformance to NRC

Regulatory Guides, and Appendix A, Table 9.5A-1. Regulatory Guide 1.39, Revision 2,

endorses ANSI Standard N45.2.3-1973, Housekeeping During the Construction Phase of

Nuclear Power Plants.

ANSI Standard N45.2.3-1973, Section 3.5 states, in part, that periodic inspection and

examination of the work areas shall be performed at scheduled intervals to assure

- 50 - Enclosure 2

adequacy of cleanliness and housekeeping practices. Section 4 states, in part, that

copies of inspection and examination records shall be prepared and placed with other

project records.

Procedure AP 12-001, Housekeeping Control, Revision 6C, dated May 5, 2006,

Section 6.1.8 required that Assigned personnel shall walk down their areas monthly

(3) These Individuals or Designees shall walk down their assigned areas monthly.

Procedure AP 12-001, Housekeeping Control, Revision 7, dated November 10, 2008,

Section 6.1.8, required that Assigned personnel shall walk down their areas monthly

[i.e., allowed use of designees was removed].

Contrary to the above, between October and December 2008, the licensee failed to

maintain records required by License Condition 2.C.5 that were complete and accurate in

all material respects. Specifically, the Housekeeping Inspection Card for the spent fuel

pool area indicated that the inspection had been completed when security access logs

indicate that the individual that completed the record had not entered the area. The NRC

investigation determined that the assigned individual did not walk down the assigned area,

and did not assign a designee to do so.

This is a violation of 10 CFR 50.9. A notice of violation is attached. NOV 05000482/2013-

08 Failure to Maintain Complete and Accurate Housekeeping Records. (EA-13-084)

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 23, 2013, the inspectors presented the results of the radiation safety inspections to

Ms. A. Stull, Vice President and Chief Administrative Officer, and other members of the licensee

staff. The licensee acknowledged the issues presented. The inspectors asked the licensee

whether any materials examined during the inspection should be considered proprietary. No

proprietary information was identified.

On June 12, 2013, the inspector debriefed the results of the review of LER 2011-008-00 to

Mr. R. Hobby, Licensing, and Mr. D. Garbee, Acting Fire Protection Supervisor. The licensee

acknowledged the issues presented. No proprietary information was reviewed.

On July 11, 2013, the resident inspectors presented the inspection results to Mr. J. Broschak,

and other members of the licensee staff. The licensee acknowledged the issues presented.

The inspector asked the licensee whether any materials examined during the inspection should

be considered proprietary. No proprietary information was identified.

On August 7, 2013, the resident inspectors conducted a supplemental exit with Mr. R.Smith to

revise the characterization of two findings. The licensee acknowledged the issues presented.

The inspector asked the licensee whether any materials examined during the inspection should

be considered proprietary. No proprietary information was identified.

- 51 - Enclosure 2

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

A. Camp, Plant Manager

A. Stull, Vice President and Chief Administrative Officer

B. Fox, Contractor, Fire Protection Engineer

D. Dees, Operations Support Superintendant

D. Grove, Maintenance Superintendant

E. Peterson, Ombudsman

G. Pendergrass, Manager Station Recovery

J. Broschak, Engineering Vice President

J. Kobyra, Manager Design Engineering

J. Schepers, Supervisor, Radiation Protection

J. Yunk, Manager Performance Improvement and Corrective Actions

K. Davis, Welder, Mechanical Maintenance

L. Aiken, Master Health Physics Technician, Radiation Protection

L. Lane, Operations Superintendant

L. Ratzlaff, Manager Maintenance

L. Upson, Manager Integrated Plant Scheduling

M. Church, Master Welder, Mechanical Maintenance

M. Skiles, Supervisor, Radiation Protection

M. Sunseri, President and Chief Executive Officer

M. Westman, Manager Regulatory Affairs

P. Bedgood, Manager Radiation Protection

P. Herrman, Manager Support Engineering

R. Clemens, Strategic Projects Vice President

R. Flannigan, Manager Nuclear Engineering

R. Hobby, Specialist, Licensing

R. Rumas, Manager Quality

R. Smith, Site Vice President and Chief Nuclear Operations Officer

S. Henry, Manager Operations

T. Baban, Manager System Engineering

T. Damashek, Operations Training Superintendent

T. East, Superintendent of Emergency Planning

T. Patten, Master Health Physics Technician, Radiation Protection

T. Slenker, Operations Corrective Action Program Coordinator

W. Muilenberg, Supervisor Licensing

A1-1 Attachment 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000482/2013003- Notice of Enforcement Discretion (NOED) 13-4-002 for a Non-

URI

07 Functional Class 1E Air Conditioning Unit (Section 4OA3.7)

Closed

05000482/2011- Post-Fire Safe Shutdown Latent Design Issue May Cause

LER

008-00 Essential Service Water System Flow Imbalance (Section 4OA3.1)

05000482/2009- Loss of Both Diesel Generators with All Fuel in the Spent Fuel

LER

005-01 Pool (Section 4OA3.8)

Movement of Irradiated Fuel Progressed After Non-Conservative

05000482/2013-

LER Decision Making Resulted in Removal of One Source Range

003-00

Monitor from Service (Section 4OA3.2)

05000482/2013- Fatigue Failure of Jacket Water Pressure Switch Diaphragm

LER

005-00 Results in Loss of the B Diesel Generator (Section 4OA3.3)

Opened and Closed

05000482/2013003-

NCV Failure to Follow Station Procedures (Section 1R08.3.b.1)

01

05000482/2013003- Failure to Identify Leakage at Refuel Pool Cavity (Section

NCV

02 1R08.3.b.2)

05000482/2013003- Diesel Generator Pressure Switch Failed Due to Instrument Line

NCV

03 Pressure Oscillations (Section 4OA3.3)

Failure to Update Station Procedures and Train Operators

05000482/2013003-

NCV Regarding the Effects of Implemented Design Changes to the

04

Main Turbine Control System (Section 4OA3.5.b.1)

Failure to Properly Manage Reactivity Changes when Swapping

05000482/2013003-

NCV Turbine Steam Admission Modes from Full to Partial Arc (Section

05

4OA3.5.b.2)

05000482/2013003- Failure to Maintain Complete and Accurate Housekeeping Records

NOV

06 (Section 4OA5)

A1-2

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

PROCEDURES

NUMBER TITLE REVISION

OFN AF-025 Unit Limitations 39

ALR 00-114D OA/OPC Trouble 5

ALR 00-134E Main Transformer Trouble 11

Section 1R04: Equipment Alignment

PROCEDURES

NUMBER TITLE REVISION

SYS KJ-125 EDG Starting Air Compressor Operation 15

CKL EF-120 Essential Service Water Valve, Breaker and Switch Lineup 46

CKL AL-120 Auxiliary Feedwater Normal Lineup 40A

DRAWINGS

NUMBER TITLE REVISION

M-12KJ05 Piping and Instrumentation Diagram, Standby Diesel 16

Generator B Intake Exhaust, F.O. & Start Air Sys.

M-11EF01 System Flow Diagram Essential Service Water 09

M-12AL01 Piping and Instrumentation Diagram Auxiliary Feedwater 23

System

CONDITION REPORTS

54654 62411 62413

WORK ORDERS

07-292792-016 07-292792-017 07-292792-021 07-292792-022 07-292792-039

07-292792-040

A1-3

Section 1R05: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

AP 10-100 Fire Protection Program 17

AP 10-106 Fire Preplans 13

DRAWINGS

NUMBER TITLE REVISION

E-1F9905 Fire hazard Analysis 4

Section 1R08: Inservice Inspection

CONDITION REPORTS

00034867 00036937 00041751 00051596

00035428 00036938 00043489 00053786

00035429 00037276 00043490 00054549

00035665 00037334 00044754 00056232

00035940 00037386 00044963 00056535

00036024 0037803 00044966 00057429

00036438 00038141 00047212 00057463

00036443 00038972 00048307 00058234

00036876 00041750 00048368 00058734

DRAWINGS

NUMBER TITLE REVISION

M-1G062 Equipment Location Turbine Building Partial Plan 2

El. 2015-4

PROCEDURES

NUMBER TITLE REVISION

AI 16F-001 Evaluation Of Boric Acid Leakage 7

AI 16F-002 Boric Acid Leakage Management 7

AP 16F-001 Boric Acid Corrosion Control Program 6B

AP 22A-001 Screening, Prioritizing, and Pre-Approval 15

AP 29A-003 Steam Generator Management 15

AP 29A-004 American Society Mechanical of Engineers (ASME) 8

Section Xi System Pressure Testing

A1-4

PROCEDURES

NUMBER TITLE REVISION

I-ENG-023 Steam Generator Data Analysis Guidelines 13

PDI ISI 254 SE NB Remote lnservice Examination of Reactor Vessel 2

Nozzle to Safe End, Nozzle to Pipe and Safe End to

Pipe Welds Using the Nozzle Scanner

PDI UT 8 PDI Generic Procedure for Ultrasonic Examination of F

Weld Overlaid Similar and Dissimilar Metal Welds

PDI-UT-1 Generic Procedure for Ultrasonic Examination of E

Ferritic Pipe Welds

QCP-20-502 Magnetic Particle Examination AC/DC Yoke and AC 8B

Coil Techniques

QCP-20-520 Pressure Test Examination 9

STN PE-040D RCS Pressure Boundary Integrity Walkdown 3

STN PE-040G Transient Event Walkdown 4

STN PE-370 Foreign Object Search and Retrieval and Secondary 12

Side Inspections

STS PE-022 Steam Generator Tube Inspection 19

STS PE-040E RPV Head Visual Inspection 3

UT 2 Ultrasonic Examination of Vessel Welds and Adjacent 28

Base Metal

UT 92 Ultrasonic Examination of Overlaid Austinetic Piping 6

Welds

UT-94 Lambert, McGill, and Thomas Nondestructive 7

Examination Procedure - Ultrasonic Examination of

Ferritic Pipe Welds

WDI STD 101 RHVI Vent Tube J-Weld Eddy Current Examination 10

WDI STD 1040 Procedure for Ultrasonic Examination of Reactor 9

Vessel Head Penetrations

WDI STD 1041 Reactor Vessel Head Penetrations Ultrasonic 8

Examination Analysis

WDI STD 114 RHVI Vent Tube ID and CS Wastage Eddy Current 12

Examination

WDI STD 146 ET Examination of Reactor Vessel Pipe Welds Inside 11

Surface

A1-5

MISCELLANEOUS

NUMBER TITLE REVISION / DATE

09-00178 Wolf Creek Generating Station - Request For March 27, 2009

Additional Information Re: Relief Request 13R-06,

Alternative To The Examination Requirements Of

ASME Section XI For Class 1 Piping Welds

Examined From The Inside Of The Reactor Vessel

(TAC No. MD9658)

ASS03 Performance Improvement Learning Oversight and September 20, 2006

Trending System Assessment/Audit Detail Report -

BACCP Self-Assessment

Code Case Alternative Examination Requirements for PWR March 28, 2006

N-729-1 Reactor Vessel Upper Heads With Nozzles Having

Pressure-Retaining Partial-Penetration Welds

Section XI, Division 1

ES1301910 Boric Acid Training for WCNOC Supervision 001

ESH - 102 STARS Plants Alloy 600 Program Review September 5, 2006

ET 06-001 0 Docket 50-482: Inservice Inspection Program Plan March 2, 2006

for the Third Ten-Year Interval and 10 CFR 50.55a

Requests 13R-01, 13R-02,and 13R-04

ET 06-0021 Docket No. 50-482: 10 CFR 50.55a Request 13R- May 9, 2006

05, Installation and Examination of Full Structural

Weld Overlays for Repairing/Mitigating Pressurizer

Nozzle-to-Safe End Dissimilar Metal Welds and

Adjacent Safe End-to-Piping Stainless Steel Welds

ET 06-0031 Docket 50-482: Wolf Creek Nuclear Operating August 4, 2006

Corporation's Response to Request for Additional

Information Regarding I 0 CFR 50.55a Request l3R-

05 and Submittal of Revision 1 to 10 CFR 50.55a

Request 13R-05

ET 060042 Docket 50-482: Wolf Creek Nuclear Operating September 27, 2006

Corporation's Response to the September 20, 2006

NRC Request for Additional Information Regarding

10 CFR 50.55a Request 13R-05

ET 06-0043 Docket 50-482: Wolf Creek Nuclear Operating October 5, 2006

Corporation's Response to NRC Request for

Additional Information Regarding 10 CFR 50.55a

Request 13R-01

ET 06-0044 Docket 50-482: Wolf Creek Nuclear Operating October 2, 2006

Corporations Revised Commitment Regarding 10

CFR 50.55a Request 13R-05

A1-6

MISCELLANEOUS

NUMBER TITLE REVISION / DATE

ET 06-0058 Docket No. 50-482: Wolf Creek Nuclear Operating December 20,2006

Corporation's Response to the Second NRC

Request for Additional Information Regarding 10

CFR 50.55a Request 13R-01

ET 08-0044 Docket No. 50-482: 10 CFR 50.55a Request 13R- September 16, 2008

06, Alternative to the Examination Requirements of

ASME Section XI for Class 1 Piping Welds

Examined from the Inside of the Reactor Vessel

ET 09-0014 Docket No. 50-482: Wolf Creek Nuclear Operating April 23, 2009

Corporation's Response to Request for Additional

Information Regarding 10 CFR 50.55a Request

13R-06

ET 12-0010 Docket 50-482: 10 CFR 50.55a Request Number July 2, 2012

13R-07, Relief from ASME Code Case N-729-1

Requirements for Examination of Reactor Vessel

Head Penetration Welds

Letter from Wolf Creek Generating Station -Request For Relief January 4, 2013

Matthew W. No. 13R-07 For The Third 10-Year Inservice

Sunseri Inspection Program Interval (TAC No. ME9078)

Letter from Wolf Creek Generating Station - Third 10-Year February 21, 2007

Rick A. Muench Interval Inservice Inspection Program Relief

Request I3R-01 (TAC No. MD0297

Letter from Wolf Creek Generating Station - Authorization Of July 19, 2007

Rick A. Muench Relief Request I3r-05, Alternatives To Structural

Weld Overlay Requirements (TAC No. MD1813)

Letter from Wolf Creek Generating Station -Relief Request July 23, 2009

Rick A. Muench 13R-06, Alternative To The Examination

Requirements Of ASME Code,Section XI For Class

1 Piping Welds Examined From The Inside Of The

Reactor Vessel (TAC No. MD9658)

Letter from NCR Wolf Creek Generating Station -Issuance Of November 19, 2012

to Matthew W. Amendment RE: Adoption of TSTF-510, Revision 2,

Sunseri "Revision To Steam Generator Program Inspection

Frequencies And Tube Sample Selection," Using

The Consolidated Line Item Improvement Process

(TAC No. ME8569)

Letter from NCR Wolf Creek Generating Station -Issuance Of December 11, 2012

to Matthew W. Amendment Re: Steam Generator Tube Permanent

Sunseri Alternate Repair Criteria (TAC No. ME8350)

A1-7

MISCELLANEOUS

NUMBER TITLE REVISION / DATE

ME9078 Request For Additional Information Request I3R-07 September 4, 2012

Examination Of Reactor Vessel Head Penetration

Welds Wolf Creek Generating Station Unit 1 Wolf

Creek Nuclear Operating Corporation Docket

Number 50-482

October 15, 2012 Docket 50-482: Response to Request for Additional October 15, 2012

Information Regarding 10 CFR 50.55a Request

Number 13R-07, "Relief from ASME Code Case N-

729-1 Requirements for Examination of Reactor

Vessel Head Penetration Welds"

SA-2012-0023 ISI Program Self Assessment March 8, 2012

SEL 2010-163 Self-Assessment Report SEL 2010-163 March 25, 2010

Steam Generator Health Optimization

SG-CDME-12-2 Wolf Creek Steam Generator Secondary Side October 2012

Condition Monitoring and Operational Assessment

for Fuel Cycle 19 and Refueling Outage 19

SG-SGDA-11-1 Wolf Creek RF18 Condition Monitoring Assessment January 2012

and Operational Assessment

Section 1R11: Licensed Operator Requalification Program

PROCEDURES

NUMBER TITLE REVISION

AP 21-001 Conduct of Operations 60

GEN 00-004 Power Operations 69

GEN 00-005 Minimum Load to Hot Standby 75

OP3003501 Steam Generator Tube Rupture Response Methodology 00

Change Lab

LR5002023 Inadvertent Safety Injection Lab 004

Section 1R12: Maintenance Effectiveness

PROCEDURES

NUMBER TITLE REVISION

AP 23M-001 WCGS maintenance Rule Program 9

A1-8

CONDITION REPORTS

68393 70858 70854 66874 ACE 51622

66244 66499 66875

WORK ORDERS

12-353867-000 13-099778 13-366342-000 13-366342-001

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

Maintenance Rule Database

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURES

NUMBER TITLE REVISION /

DATE

AP 22C-003 Online Nuclear Safety and Generation Risk Assessment 19

APF 22C-003-01 On-Line Nuclear Safety and Generation Risk Assessment May 20, 2013

Week (2013) 208 (as revised)

MISCELLANEOUS

NUMBER TITLE REVISION

Work Week 2013-205 Major Activities (4/29-5/05) 0

Work Week 13-202 Risk Assessment 0

Section 1R15: Operability Evaluations

PROCEDURES

NUMBER TITLE REVISION

AP 06-002 Radiological Emergency Response Plant (RERP) - 13

Emergency Action Level -1 Radioactive Effluent Release

AP 26C-004 Operability Determination and Functionality Assessment 26

AI 22C-016 Unit Condition and Operational Residual Risk 0A

AI 22C-010 Operations Work Controls 15

STS AL-103 TDAFW Pump Inservice Test 57

A1-9

CONDITION REPORTS

00062146 00064397 00067888 66396 66398

00057299 00063495

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

13-364867-001 Engineering Disposition: Justification of AFW Pump PAL02 March 8,

Stuffing Box Extension Through-Wall 2013

13-365489-001 Engineering Disposition: PEJ01A Diffuser Volute Vane 2

Damage

13-366890-000 & Engineering Disposition: PEM01A/B Operated With No 0

13-366291-000 Suction Sources

Interim Operation Assessment: PEM01A (SI pump A) April 18,

2013

Interim Operation Assessment: PEM01B (SI pump B) April 8, 2013

GK-13-004 Operability Evaluation: SGK05A Class 1E AC Unit A 0

Engineering Disposition: ESC - PEM01A/B Operated With 0

No Suction Sources

Section 1R18: Plant Modifications

TEMPORARY MODIFICATION ORDER

NUMBER TITLE REVISION

13-003-KE Removal of Fuel Transfer System Hold Down Assembly 0

DOCUMENTS

NUMBER TITLE REVISION /

DATE

DCP 14263 SBO Diesel Generator Project- Missile Barrier Erection and 4

Equipment Installation Work Outside Protected Area

DCP 12958 Turbine Driven Auxiliary Feedwater Pump Governor Control 9

Modification

A1-10

DOCUMENTS

NUMBER TITLE REVISION /

DATE

WCAP-17100-P PRA Model for the Westinghouse Shutdown Seal, 0

Supplement 1

WCAP-17541-P Implementation Guide for Westinghouse Reactor Coolant 0

Pump SHIELD Passive Thermal Seal

AI 21-017 Timed Fire Protection Actions Validation 4

MPM M712Q-01 Reactor Coolant Pump Seal Removal/Installation 23

XX-E-013-002 Post-fire Safe Shutdown (PFSSD) Analysis 19

WCOP-24 Operations EMG/OFN Setpoints 11

OFN BB-005 RCP Malfunctions 21

RCP Vendor Technical Manual 6

MGE TL-001 Wiring Termination and Lug/Connector Installation 19

AP 16E-002 Post maintenance Testing Development 13

2013-432 Breach Permit April 15,

2013

OE NB-13-002 Operability Evaluation NB001, NB002 0

QR-03117685-1 Qualification Report for Current Transformer and Modified 2

Bus Installation for General Electric Type M26 Switchgear

Technical Review of NB-13-02 0

AP 10-104 Breach Authorization 27

A1-11

DRAWINGS

NUMBER TITLE REVISION

WIP-E-13NB03- Lower Medium Voltage Sys. Class 1E 4.16KV Three Line 1-6

005-A-1 Meter and Relay Diagram

WIP-E- Schematic Diagram Class 1E Bus NB)! Feeder BRKR. 0

13KUO1A-000- 152NB0114

A-1

WIP-E-009- MetalClad Switchgear Connection Diagram 1

00132-W08-A-1

WIP-E-009- Electrical Diagram: Power Control Circuits 1

00024-W11-A-1

M-712-00206 Shutdown Seal Model 93A-1 & 100 RCP Shutdown Seal 1

Assembly Components

M-712-00207 No. 1 Seal Assembly Kit 8 inch 1

M-712-00056 General Assembly 93A-1 R.C. Pump 16

M-712-00057 General Assembly 93A-1 R.C. Pump 11

M-712-00058 General Assembly 93A-1 R.C. Pump 9

M-712-00059 General Assembly 93A-1 R.C. Pump 15

Work in Progress Drawings Associated with DCP 14117

Work in Progress Drawings Associated with DCP 14261

Work in Progress Drawings Associated with DCP 14262

Work in Progress Drawings Associated with DCP 14263

A1-12

WORK ORDERS

12-350886-025 12-350886-026 12-350886-027 12-350886-028 12-350886-029

12-350886-030 12-350886-031 12-350886-032 12-354257-003 12-354257-063

12-361102-016 12-354257-006 12-354257-126 12-354257-128 12-354257-129

CONDITION REPORTS

66117 65321 63243 66592 66698

MISCELLANEOUS

NUMBER TITLE REVISION

USAR 15.7.4 Fuel Handling Accidents 21

Section 1R19: Post-Maintenance Testing

PROCEDURES

NUMBER TITLE REVISION

MPE BA 014 Battery Impedance Test 4A

MPE E050Q-05 Battery Equalizing Procedure 13A

STS MT-019 125VDC Class 1E Quarterly Battery Inspection 21

STS MT-020 125 Volt DC Battery Inspection/Charger Operational Test 25B

STS MT-021 Service Test for 125Vdc Class 1E Batteries 16A

STS EF-100B ESW Pump B In-service Test and Discharge Check Valve 40

In-service Test

SYS GK-123 Control Building A/C Units Startup and Shutdown 21

STS IC-565 Channel Calibration Auxiliary Feedwater Pump Suction 5A

Pressure Indication for Remote Shutdown Pressure

CNT-MM-700 Fabrication and Installation of Tubing, Tubing Supports, 5

Instrument Supports and Instrument Installation

MPE GK-003 Control Room and Class 1E A/C Units Preventive 4

Maintenance Activity

MPE GK-004 GK Unit Preparation for Work 4

A1-13

CONDITION REPORTS

70420 ACE 19528 67888 66398 66396

57299

WORK ORDERS

11-340517-002 11-341224-001 09-321171-001 11-341337-002 11-342032-004

08-309413-041 09-342741-002 11-341336-003 11-345398-002 09-317266-001

11-343552-002 11-343567-001 12-353040-003 11-345397-002 11-337095-005

11-343332-000 11-343334-000 12-352686-000 13-373150-004 10-333747-000

13-373150-002 12-352686-000 13-373153-001 13-373153-009 12-361695-005

13-373153-008 13-373153-004 13-373153-000

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

Balance of Plant Eddy Current Inspection Report EEC01A June 20,

Spent Fuel Pool Cooler 2013

M-071-0016-05 Vendor Manual: Cooling the Spent Fuel Pool 3

M-071-0015-03 Vendor Manual: Exchange Surface Requirement Based on May 12, 1977

Case A Conditions

V5011748 SGKOSA Oil Analysis Certificate, Herguth Laboratories June 26,

2013

V5011749 SGKOSA Oil Analysis Certificate, Herguth Laboratories June 26,

2013

Section 1R20: Refueling and Other Outage Activities

PROCEDURES

NUMBER TITLE REVISION

GEN 00-003 Hot Standby to Minimum Load 87A

RXE 01-002 Reload Low Power Physics Testing 24

CONDITION REPORTS

00064552 00063645

A1-14

MISCELLANEOUS

NUMBER TITLE REVISION

Reactivity Maneuver Plan, Cycle 20 Initial Startup 0

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION

STS KJ-001A Integrated Diesel Generator and Safeguards Actuation Test 48A

Train A

STS KJ-001B Integrated Diesel Generator and Safeguards Actuation Test 47A

Train B

STS KJ-005A Manual/Auto Start, Synch, & Loading of EDG NE01 58

STN AL-100C TDAFW Pump Reference Pump Curve Determination 1

STS IC-201A Channel Operational Test of Tavg, T and Pressurizer 18

Pressure Protection Set One

STS AB-201B TDAFP Steam Isolation Inservice Valve Test 8

STS AL-201C Turbine Driven Auxiliary Feedwater System Inservice Valve 8

Test

DRAWINGS

NUMBER TITLE REVISION

J-14K81 Compressed Air System Auxiliary Building Details 3

M-12KA05 Piping and Instrumentation Diagram Compressed Air 7

System

M-12AL01 Piping and Instrumentation Diagram Auxiliary Feedwater 23

System

CONDITION REPORTS

00068192 00068267 00068271 00068274 00067526

00060210

WORK ORDER

12-361011-000

A1-15

Section 2RS2: Occupational ALARA Planning and Controls

PROCEDURES

NUMBER TITLE REVISION

AI 16C-008 Work Order Implementation 20A

AI 16C-012 Refuel Preparation & Walk down Guidelines 5

AP 05-009 ALARA Design Guidelines 2A

AP 16C-006 MPAC Work Request / Work Order Process Controls 21

AP 25A-401 ALARA Program 21

AP 25A-410 ALARA Committee 16

AP 25B-300 RWP Program 22

RPP 02-105 RWP 37

RADIATION WORK PERMITS

NUMBER TITLE REVISION

131000 Health Physics Rover Coverage for RF-19s 2

132001 Mechanical Maintenance Welding Department RWP 5

132002 Maintenance Expanded Scope 6

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER TITLE DATE

12-03-RP/PC Radiation Protection/Process Control Programs May 4, 2012

CORRECTIVE ACTION DOCUMENT NUMBERS

64705 65144 65145 65148 65422

65517

WORK ORDERS

09-316582-014 09-346910-000 11-346910-006

A1-16

MISCELLANEOUS DOCUMENTS

NUMBER TITLE DATE

Official Dose for 2010 April 13, 2013

Official Dose for 2011 April 13, 2013

Official Dose for 2012 April 13, 2013

Three Year Rolling Average April 16, 2013

Wolf Creek ALARA Long Range Exposure /Source Term January 10, 2012

Reduction Plan for 2011 - 2016

131000 ALARA Review June, 27, 2012

131000 Post Job ALARA Review April 17, 2013

131000 RWP Budget Report April 17, 2013

132001 ALARA Review December 10,

2012

132001 Post Job ALARA Review May 16, 2013

132001 RWP Budget Report April 18, 2013

132002 ALARA Review February 27, 2013

132002 Post Job ALARA Review April 22, 2013

132002 RWP Budget Report April 15, 2013

Section 2RS4: Occupational Dose Assessment

PROCEDURES

NUMBER TITLE REVISION

RPP 03-121 Neutron Dose Calculations 5

RPP 03-122 Skin Dose Calculations 12

RPP 03-205 DAC-Hour Tracking 16

RPP 03-210 Internal Exposure Calculations and Evaluations 14A

RPP 03-215 Collection of Bioassay Samples 5

RPP 03-406 HP Dosimetry/Records 9

RPP 03-407 Testing of Portal Monitors as Passive Whole Body Counters 1A

A1-17

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER TITLE DATE

12-03-RP/PC Radiation Protection / Process Control Program May 4, 2012

CONDITION REPORTS

64625 65544 65925

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION / DATE

APF 30E-OOR- Site Access Training Site Specific - Lesson Plan 6

01

List of RWP Tasks with Multi-Packs May 23, 2013

List of Multipacks per RCA Entry May 23, 2013

Form RPF 03-406 2

Section 4OA1: Performance Indicator Verification

PROCEDURE

NUMBER TITLE REVISION

NEI 99-02 Reactor Oversight Process Performance Indicators 9

Section 4OA2: Identification and Resolution of Problems

CONDITION REPORT

00062234 00025515 00046239 43270 000543

00064461 00064464 00065305 00065418 00065421

00065430 00065799

MISCELLANEOUS

NUMBER TITLE DATE

Wolf Creek Generating Station: Station Roll-up February 4,

Performance Results, 4th Quarter 2012 2013

Wolf Creek Generating Station: Station Roll-up May 6, 2013

Performance Results, 1st Quarter 2013

A1-18

Section 4OA3: Event Follow-Up

PROCEDURES

NUMBER TITLE REVISION

MPM M018Q-01 Standby Diesel Generator Inspection 20

SYS KJ-124 Post Maintenance Run of Emergency Diesel Generator B 52

STS KJ-001B Integrated D/G and Safeguards Actuation Test - Train B 47

STS AC-001 Main Turbine Valve Cycle Test 36

TMP 12-016 Post Modification Main Turbine Control System Generator 7

Startup and Testing

AI 28A-010 Screening Condition Reports 15

AP 05-005 Design, Implementation & Configuration Control of 19

Modifications

AP 19E-002 Reactivity Management Program 17

AP 21-001 Conduct of Operations 61

PROCEDURES

NUMBER TITLE DATE

13-0449 CKL ZL-005A: A EDG Operating Log Rev 4 March 3,

2013

13-0471 CKL ZL-005B: B EDG Operating Log Rev 5 March 3,

2013

13-0567 SYS KJ-123: Post Maintenance Run of Emergency Diesel March 4,

Generator A Rev 53 2013

13-0568 SYS KJ-124: Post Maintenance Run of Emergency Diesel March 4,

Generator B Rev 53 2013

13-0570 MPM M018Q-01: Standby Diesel Generator Inspection Rev March 7,

22 2013

13-0653 SYS KJ-121: Diesel Generator NE01 and NE02 Lineup for March 3,

Automatic Operation Rev 46 2013

CONDITION REPORTS

00064828 65624 67538 67528 67582

67623 70814 68711 68720 68556

70789

A1-19

WORK ORDER

13-365878-002

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

EN# 48802 NOUE: both diesel generators unavailable 3/1/2013

2009-005 Licensee Event Report: Loss of both Diesel Generators 01

with all Fuel in the Spent Fuel Pool

2013-003 Licensee Event Report: Movement of Irradiated Fuel 00

Progressed After Non-Conservative Decision Making

Resulted in Removal of One Source Range Monitor From

Service

2013-005 Licensee Event Report: Fatigue Failure of Jacket Water 00

Pressure Switch Diaphragm Results in Loss of the B Diesel

Generator

WOL-52624 Failure Analysis of SOR Pressure Switch Manufacturer: April 10,

SOR, Model: 4N6-B5-NX-01A-JJTTX12 Purchase Order 2013

No.: 764426, Exelon Power Labs

Control Room Log March 13,

2013

M-018-01387 Vendor Manual: Installation Operating and Maintenance September

W03 Instructions for Model 20 Air Volume Booster 27, 2005

Fire Event Investigation Report: Auxiliary Boiler Roof April 11, 2013

adjacent to exhaust stack penetration

EN# 48914 Fire Lasting Greater Than 15 Minutes April 11, 2013

DESIGN AND LICENSEE BASIS DOCUMENTS

NUMBER TITLE REVISION

013898 PFSSD - EFHV0060 Control Wiring Modification 0

A1-20

DRAWINGS

NUMBER TITLE REVISION

WIP-E-13EF04A- ESW From Component Cooling Water Heat Exch. Iso. Valve 00

000-A-1, Sh 1 EFHV0060

WIP-E-025- ESW B Return from CCW Heat Exchanger B 0

00007-W13-

A-199

M-12KJ01 Piping & Instrumentation Diagram Standby Diesel 12

Generator Cooling Water System

M-12KJ04 Piping & Instrumentation Diagram Standby Diesel 16

Generator B Cooling Water System

Section 4OA5: Other Activities

WORK ORDERS

12-356794-001 12-356794-003 12-356794-008 12-356794-012

MISCELLANEOUS

NUMBER TITLE DATE

ET 12-0015 Wolf Creek Letter from J. Broschak to U.S. NRC, Re: July 2, 2012

Seismic Aspects of Recommendation 2.3 of the Near-Term

Task Force Review of the Fukushima Dai-ichi Accident

ET 12-0031 Wolf Creek Letter from J. Broschak to U.S. NRC, Re: 180 November

day response to Recommendation 2.3 of the Near-Term 27, 2012

Task Force Review of the Fukushima Dai-ichi Accident

EPRI 1025286 Seismic Walkdown Guidance June 2012

A1-21

Request for Information for Inservice Inspection

Wolf Creek Nuclear Power Plant

February 11, 2013, through February 22, 2013

NRC Inspection Report 05000482/2013002

Please provide the requested information. Thank you for your support.

NOTE: In an effort to keep the requested information organized, please submit the

information using the same request designation. For example, the names and

phone numbers for the program leads should be in a file/folder titled A.5.b.

If you have any questions or comments, please contact the lead inspector Ronald Kopriva at

(817) 200-1104 (Ron.Kopriva@nrc.gov )

PAPERWORK REDUCTION ACT STATEMENT

This letter does not contain new or amended information collection requirements

subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.).

Existing information collection requirements were approved by the Office of

Management and Budget, control number 3150-0011.

A2-1 Attachment 2

INSERVICE INSPECTION DOCUMENT REQUEST

Inspection Dates: February 11 through February 22, 2013

Inspection Procedures: IP 71111.08 Inservice Inspection (ISI) Activities

Inspectors: Ronald Kopriva, Senior Reactor Inspector (Team Lead)

Megan Williams, Reactor Inspector

A. Information Requested for the In-Office Preparation Week

The following information should be sent to the Region IV office in hard copy or

electronic format (ims.certrec.com preferred), in care of Ronald Kopriva, by February

1, 2013, to facilitate the selection of specific items that will be reviewed during the onsite

inspection week. The inspectors will select specific items from the information requested

below and then request from your staff additional documents needed during the onsite

inspection week (Section B of this enclosure). We ask that the specific items selected

from the lists be available and ready for review on the first day of inspection. Please

provide requested documentation electronically if possible. If requested documents are

large and only hard copy formats are available, please inform the inspector(s), and

provide subject documentation during the first day of the onsite inspection. If you have

any questions regarding this information request, please call the inspector as soon as

possible.

A.1 ISI/Welding Programs and Schedule Information

a) A detailed schedule (including preliminary dates) of:

i) Nondestructive examinations planned for Class 1 & 2 systems and

containment, performed as part of your ASME Section XI, risk informed (if

applicable), and augmented inservice inspection programs during the

upcoming outage.

Provide a status summary of the nondestructive examination inspection

activities vs. the required inspection period percentages for this interval

by category per ASME Section XI, IWX-2400. Do not provide separately

if other documentation requested contains this information.

ii) Reactor pressure vessel head examinations planned for the upcoming

outage.

iii) Examinations planned for Alloy 82/182/600 components that are not

included in the Section XI scope (If applicable).

iv) Examinations planned as part of your boric acid corrosion control

program (Mode 3 walkdowns, bolted connection walkdowns, etc.).

A2-2

v) Welding activities that are scheduled to be completed during the

upcoming outage (ASME Class 1, 2, or 3 structures, systems, or

components).

b) A copy of ASME Section XI Code Relief Requests and associated NRC safety

evaluations applicable to the examinations identified above.

c) A list of nondestructive examination reports (ultrasonic, radiography, magnetic

particle, dye penetrant, Visual VT-1, VT-2, and VT-3), which have identified

relevant conditions on Code Class 1 & 2 systems since the beginning of the last

refueling outage. This should include the previousSection XI pressure test(s)

conducted during start up and any evaluations associated with the results of the

pressure tests. Also, include in the list the nondestructive examination reports

with relevant conditions in the reactor pressure vessel head penetration nozzles

that have been accepted for continued service. The list of nondestructive

examination reports should include a brief description of the structures, systems,

or components where the relevant condition was identified.

d) A list with a brief description (e.g., system, material, pipe size, weld number, and

nondestructive examinations performed) of the welds in Code Class 1 and 2

systems which have been fabricated due to component repair/replacement

activities since the beginning of the last refueling outage, or are planned to be

fabricated this refueling outage.

e) If reactor vessel weld examinations required by the ASME Code are scheduled to

occur during the upcoming outage, provide a detailed description of the welds to

be examined and the extent of the planned examination. Please also provide

reference numbers for applicable procedures that will be used to conduct these

examinations.

f) Copy of any 10 CFR Part 21 reports applicable to your structures, systems, or

components within the scope of Section XI of the ASME Code that have been

identified since the beginning of the last refueling outage.

g) A list of any temporary noncode repairs in service (e.g., pinhole leaks).

h) Please provide copies of the most recent self-assessments for the inservice

inspection, welding, and Alloy 600 programs.

A.2 Reactor Pressure Vessel Head (RPVH)

a) Provide the detailed scope of the planned nondestructive examinations of the

reactor vessel head which identifies the types of nondestructive examination

methods to be used on each specific part of the vessel head to fulfill

commitments made in response to NRC Bulletin 2002-02 and

NRC Order EA-03-009. Also, include examination scope expansion criteria and

planned expansion sample sizes if relevant conditions are identified. (If

applicable)

A2-3

b) A list of the standards and/or requirements that will be used to evaluate

indications identified during nondestructive examination of the reactor vessel

head (e.g., the specific industry or procedural standards which will be used to

evaluate potential leakage and/or flaw indications).

A.3 Boric Acid Corrosion Control Program

a) Copy of the procedures that govern the scope, equipment and implementation of

the inspections required to identify boric acid leakage and the procedures for

boric acid leakage/corrosion evaluation.

b) Please provide a list of leaks (including Code class of the components) that have

been identified since the last refueling outage and associated corrective action

documentation. If during the last cycle, the unit was shutdown, please provide

documentation of containment walkdown inspections performed as part of the

boric acid corrosion control program.

c) Please provide a copy of the most recent self-assessment performed for the

boric acid corrosion control program.

A.4 Steam Generator Tube Inspections

a) A detailed schedule of:

i) Steam generator tube inspection, data analyses, and repair activities for

the upcoming outage (If occurring).

ii) Steam generator secondary side inspection activities for the upcoming

outage. (If occurring).

b) Please provide a copy of your steam generator inservice inspection program and

plan. Please include a copy of the operational assessment from last outage and

a copy of the following documents as they become available:

i) Degradation assessment

ii) Condition monitoring assessment

c) If you are planning on modifying your Technical Specifications such that they are

consistent with Technical Specification Task Force Traveler TSTF-449, Steam

Generator Tube Integrity, please provide copies of your correspondence with the

NRC regarding deviations from the standard technical specifications.

d) Copy of steam generator history documentation given to vendors performing

eddy current testing of the steam generators during the upcoming outage.

A2-4

e) Copy of steam generator eddy current data analyst guidelines and site validated

eddy current technique specification sheets. Additionally, please provide a copy

of EPRI Appendix H, Examination Technique Specification Sheets, qualification

records.

f) Identify and quantify any steam generator tube leakage experienced during the

previous operating cycle. Also provide documentation identifying which steam

generator was leaking and corrective actions completed or planned for this

condition (If applicable).

g) Provide past history of the condition and issues pertaining to the secondary side

of the steam generators (including items such as loose parts, fouling, top of tube

sheet condition, crud removal amounts, etc.)

h) Provide copies of your most recent self assessments of the steam generator

monitoring, loose parts monitoring, and secondary side water chemistry control

programs.

i) Indicate where the primary, secondary, and resolution analyses are scheduled to

take place.

j) Provide a summary of the scope of the steam generator tube examinations,

including examination methods such as Bobbin, Rotating Pancake, or Plus Point,

and the percentage of tubes to be examined. Do not provide these documents

separately if already included in other information requested.

A.5 Additional Information Related to all Inservice Inspection Activities

a) A list with a brief description of inservice inspection, boric acid corrosion control

program, and steam generator tube inspection related issues (e.g., condition

reports) entered into your corrective action program since the beginning of the

last refueling outage (for Unit 2). For example, a list based upon data base

searches using key words related to piping or steam generator tube degradation

such as: inservice inspection, ASME Code,Section XI, NDE, cracks, wear,

thinning, leakage, rust, corrosion, boric acid, or errors in piping/steam generator

tube examinations.

b) Please provide names and phone numbers for the following program leads:

Inservice inspection (examination, planning)

Containment exams

Reactor pressure vessel head exams

Snubbers and supports

Repair and replacement program

Licensing

Site welding engineer

Boric acid corrosion control program

A2-5

Steam generator inspection activities (site lead and vendor contact)

B. Information to be Provided Onsite to the Inspector(s) at the Entrance Meeting

(February 11, 2013):

B.1 Inservice Inspection / Welding Programs and Schedule Information

a) Updated schedules for inservice inspection/nondestructive examination activities,

including steam generator tube inspections, planned welding activities, and

schedule showing contingency repair plans, if available.

b) For ASME Code Class 1 and 2 welds selected by the inspector from the lists

provided from section A of this enclosure, please provide copies of the following

documentation for each subject weld:

i) Weld data sheet (traveler)

ii) Weld configuration and system location

iii) Applicable Code Edition and Addenda for weldment

iv) Applicable Code Edition and Addenda for welding procedures

v) Applicable weld procedures used to fabricate the welds

vi) Copies of procedure qualification records supporting the weld procedures

from B.1.b.v

vii) Copies of mechanical test reports identified in the procedure qualification

records above

viii) Copies of the nonconformance reports for the selected welds (If

applicable)

ix) Radiographs of the selected welds and access to equipment to allow

viewing radiographs (If radiographic testing was performed)

x) Copies of the preservice examination records for the selected welds

xi) Copies of welder performance qualifications records applicable to the

selected welds, including documentation that welder maintained

proficiency in the applicable welding processes specified in the weld

procedures (at least 6 months prior to the date of subject work)

xii) Copies of nondestructive examination personnel qualifications (Visual

inspection, penetrant testing, ultrasonic testing, radiographic testing), as

applicable

c) For the inservice inspection related corrective action issues selected by the

inspectors from section A of this enclosure, provide a copy of the corrective

actions and supporting documentation.

d) For the nondestructive examination reports with relevant conditions on Code

Class 1 and 2 systems selected by the inspectors from Section A above, provide

a copy of the examination records, examiner qualification records, and

associated corrective action documents.

A2-6

e) A copy of (or ready access to) most current revision of the inservice inspection

program manual and plan for the current Interval.

f) For the nondestructive examinations selected by the inspectors from section A of

this enclosure, provide a copy of the nondestructive examination procedures

used to perform the examinations (including calibration and flaw

characterization/sizing procedures). For ultrasonic examination procedures

qualified in accordance with ASME Section XI, Appendix VIII, provide

documentation supporting the procedure qualification (e.g., the EPRI

performance demonstration qualification summary sheets). Also, include

qualification documentation of the specific equipment to be used (e.g., ultrasonic

unit, cables, and transducers including serial numbers) and nondestructive

examination personnel qualification records.

B.2 Reactor Pressure Vessel Head

a) Provide the nondestructive personnel qualification records for the examiners who

will perform examinations of the reactor pressure vessel head.

b) Provide drawings showing the following: (If a visual examination is planned for

the upcoming refueling outage)

i) Reactor pressure vessel head and control rod drive mechanism nozzle

configurations

ii) Reactor pressure vessel head insulation configuration

Note: The drawings listed above should include fabrication drawings for

the nozzle attachment welds as applicable.

c) Copy of nondestructive examination reports from the last reactor pressure vessel

head examination.

d) Copy of evaluation or calculation demonstrating that the scope of the visual

examination of the upper head will meet the 95 percent minimum coverage

required by NRC Order EA-03-009 (If a visual examination is planned for the

upcoming refueling outage).

e) Provide a copy of the procedures that will be used to identify the source of any

boric acid deposits identified on the reactor pressure vessel head. If no explicit

procedures exist which govern this activity, provide a description of the process

to be followed including personnel responsibilities and expectations.

f) Provide a copy of the updated calculation of effective degradation years for the

reactor pressure vessel head susceptibility ranking.

g) Provide copy of the vendor qualification report(s) that demonstrates the detection

capability of the nondestructive examination equipment used for the reactor

pressure vessel head examinations. Also, identify any changes in equipment

A2-7

configurations used for the reactor pressure vessel head examinations which

differ from that used in the vendor qualification report(s).

B.3 Boric Acid Corrosion Control Program

a) Please provide boric acid walkdown inspection results, an updated list of boric

acid leaks identified so far this outage, associated corrective action

documentation, and overall status of planned boric acid inspections.

b) Please provide any engineering evaluations completed for boric acid leaks

identified since the end of the last refueling outage. Please include a status of

corrective actions to repair and/or clean these boric acid leaks. Please identify

specifically which known leaks, if any, have remained in service or will remain in

service as active leaks.

B.4 Steam Generator Tube Inspections

a) Copies of the Examination Technique Specification Sheets and associated

justification for any revisions.

b) Copy of the guidance to be followed if a loose part or foreign material is identified

in the steam generators.

c) Please provide a copy of the eddy current testing procedures used to perform the

steam generator tube inspections (specifically calibration and flaw

characterization/sizing procedures, etc.). Also include documentation for the

specific equipment to be used.

d) Please provide copies of your responses to NRC and industry operating

experience communications such as Generic Letters, Information Notices, etc.

(as applicable to steam generator tube inspections) Do not provide these

documents separately if already included in other information requested such as

the degradation assessment.

e) List of corrective action documents generated by the vendor and/or site with

respect to steam generator inspection activities.

B.5 Codes and Standards

a) Ready access to (i.e., copies provided to the inspector(s) for use during the

inspection at the onsite inspection location, or room number and location where

available):

i) Applicable Editions of the ASME Code (Sections V, IX, and XI) for the

inservice inspection program and the repair/replacement program.

ii) EPRI and industry standards referenced in the procedures used to

perform the steam generator tube eddy current examination.

A2-8

Inspector Contact Information:

Ronald Kopriva

Senior Reactor Inspector

817-200-1104

Ron.Kopriva@nrc.gov

Mailing Address:

US NRC Region IV

Attn: Ronald Kopriva

1600 E. Lamar Blvd

Arlington, TX 76011

A2-9

The following items are requested for the

Occupational Radiation Safety Inspection

at Wolf Creek Generating Plant

May 20-24, 2013

Integrated Report 2013003

Inspection areas are listed in the attachments below.

Please provide the requested information on or before May 3, 2013.

Please submit this information using the same lettering system as below. For example, all

contacts and phone numbers for Inspection Procedure 71124.01 should be in a file/folder titled

1- A, applicable organization charts in file/folder 1- B, etc.

If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at

least 30 days later than the onsite inspection dates, so the inspectors will have access to the

information while writing the report.

In addition to the corrective action document lists provided for each inspection procedure listed

below, please provide updated lists of corrective action documents at the entrance meeting.

The dates for these lists should range from the end dates of the original lists to the day of the

entrance meeting.

If more than one inspection procedure is to be conducted and the information requests appear

to be redundant, there is no need to provide duplicate copies. Enter a note explaining in which

file the information can be found.

If you have any questions or comments, please contact Larry Ricketson at (817) 200-1165 or

Larry.Ricketson@nrc.gov.

PAPERWORK REDUCTION ACT STATEMENT

This letter does not contain new or amended information collection requirements subject

to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.). Existing information

collection requirements were approved by the Office of Management and Budget,

control number 3150-0011.

A3-1 Attachment 3

2. Occupational ALARA Planning and Controls (71124.02)

Date of Last Inspection: September 24, 2012

A. List of contacts and telephone numbers for ALARA program personnel

B. Applicable organization charts

C. Copies of audits, self-assessments, and LERs, written since date of last inspection,

focusing on ALARA

D. Procedure index for ALARA Program

E. Please provide specific procedures related to the following areas noted below.

Additional Specific Procedures may be requested by number after the inspector reviews

the procedure indexes.

1. ALARA Program

2. ALARA Committee

3. Radiation Work Permit Preparation

F. A summary list of corrective action documents (including corporate and subtiered

systems) written since date of last inspection, related to the ALARA program. In addition

to ALARA, the summary should also address Radiation Work Permit violations,

Electronic Dosimeter Alarms, and RWP Dose Estimates

NOTE: The lists should indicate the significance level of each issue and the search

criteria used. Please provide documents which are searchable.

G. List of work activities greater than 1 rem, since date of last inspection.

Include original dose estimate and actual dose.

H. Site dose totals and 3-year rolling averages for the past 3 years (based on dose of

record)

I. Outline of source term reduction strategy

A3-2

4. Occupational Dose Assessment (Inspection Procedure 71124.04)

Date of Last Inspection: August 15, 2011

A. List of contacts and telephone numbers for the following areas:

1. Dose Assessment personnel

B. Applicable organization charts

C. Audits, self assessments, vendor or NUPIC audits of contractor support, and LERs

written since date of last inspection, related to:

1. Occupational Dose Assessment

D. Procedure indexes for the following areas

1. Occupational Dose Assessment

E. Please provide specific procedures related to the following areas noted below.

Additional Specific Procedures will be requested by number after the inspector reviews

the procedure indexes.

1. Radiation Protection Program

2. Radiation Protection Conduct of Operations

3. Personnel Dosimetry Program

4. Radiological Posting and Warning Devices

5. Air Sample Analysis

6. Performance of High Exposure Work

7. Declared Pregnant Worker

8. Bioassay Program

F. List of corrective action documents (including corporate and subtiered systems) written

since date of last inspection, associated with:

1. NVLAP accreditation

2. Dosimetry (TLD/OSL, etc.) problems

3. Electronic alarming dosimeters

4. Bioassays or internally deposited radionuclides or internal dose

5. Neutron dose

NOTE: The lists should indicate the significance level of each issue and the search

criteria used.

G. List of positive whole body counts since date of last inspection, names redacted if

desired

H. Part 61 analyses/scaling factors

A3-3