ML113040031

From kanterella
Jump to navigation Jump to search
IR 05000338-11-011 and 05000339-11-011; IR 07200016-11-001 and 07200056-11-002, 08/30/2011 Through 10/03/2011, North Anna Power Station, Units 1 and 2; Augmented Inspection Team
ML113040031
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 10/31/2011
From: Mccree V
Region 2 Administrator
To: Heacock D
Virginia Electric & Power Co (VEPCO)
References
IR-11-002, IR-11-011, IR-11-001
Download: ML113040031 (101)


See also: IR 05000338/2011011

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

October 31, 2011

Mr. David A. Heacock

President and Chief Nuclear Officer

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA 23060

SUBJECT: NORTH ANNA POWER STATION - AUGMENTED INSPECTION TEAM (AIT)

REPORT 05000338/2011011, 05000339/2011011, 07200016/2011001, and

07200056/2011002

Dear Mr. Heacock:

On October 3, 2011, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection

at your North Anna Power Station Units 1 and 2, and the North Anna Independent Spent Fuel

Storage Installation. The enclosed report documents the inspection results, which were

discussed with you and other members of your staff during a public exit meeting on October 3,

2011.

On August 23, 2011, at 2:03 p.m., Eastern Daylight Time (EDT), North Anna Power Station

declared an Alert due to significant seismic activity onsite from a 5.8 magnitude earthquake that

was centered several miles from the plant. Both units experienced automatic reactor trips from

100 percent power. All offsite electrical power to the site was lost. All four emergency diesel

generators automatically started, loaded and provided power to the emergency buses. All of the

control rods inserted into the core. Decay heat was removed via the steam dumps to the

atmosphere.

At about 2:40 p.m., EDT, plant operators stopped the 2H emergency diesel generator after

observing a cooling water leak and rising temperatures on the diesel engine. The stations

blackout diesel generator was subsequently aligned to power the 2H vital bus. Offsite power

sources were restored. Both units were brought to cold shutdown for further inspection and

repairs. Damage to several onsite non-vital transformers was noted.

Because of evidence that the seismic event may have exceeded the plants design basis, and

due to the risk significance of the operational event, the NRC dispatched an Augmented

Inspection Team to the site to gather additional information and conduct a review of the event.

The team found that: (1) your operators responded to the event in a manner that protected

public health and safety; (2) ground movement during the earthquake exceeded the sites

licensed design basis; (3) no significant damage to the plant was identified; (4) safety system

functions were maintained; and (5) some equipment issues were revealed as a result of the

VEPCO 2

event. Issues requiring additional follow-up are documented as unresolved items in the

enclosed report.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Victor M. McCree

Regional Administrator

Dockets: 50-338, 50-339, 72-16, 72-56

Licenses: NPF-4, NPF-7, SNM-2507, COC-1004

Enclosure: Inspection Report 05000338/2011011, 05000339/2011011, 07200016/2011001,

and 07200056/2011002

w/ Attachments: 1. Supplemental Information

2. Sequence of Events

3. Augmented Inspection Team Charter

4. Public Exit Meeting Slides

cc w/ encl. (See next page)

_ML113040031________ X SUNSI REVIEW COMPLETE X FORM 665 ATTACHED

OFFICE RII:DRP RII:DRP RII:DRP RII:DRS RII:RA RII:DRP RII:DRS

SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ RA By E-mail/ /RA/

NAME SNinh GMcCoy RCroteau MFranke LWert GKolcum SWalker

DATE 10/13/2011 10/18/2011 10/20/2011 10/19/2011 10/26/2011 10/06/2011 10/06/2011

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRS RII:NRR RII:DCP HQ:NRO HQ:NRO RII:DRS

SIGNATURE RA By E-mail/ RA By E-mail/ RA By E-mail/ RA By E-mail/ RA By E-mail/ /RA By

HChristensen/

NAME LSuggs YLI RJackson MChakravorty SPark JMunday

DATE 10/06/2011 10/06/2011 10/06/2011 10/05/2011 10/06/2011 10/18/2011

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

VEPCO 3

cc w/encl: Michael M. Cline

Larry Lane Director

Site Vice President Virginia Department of Emergency Services

North Anna Power Station Management

Virginia Electric & Power Company Electronic Mail Distribution

Electronic Mail Distribution

Executive Vice President

Fred Mladen Old Dominion Electric Cooperative

Director, Station Safety & Licensing Electronic Mail Distribution

Virginia Electric and Power Company

Electronic Mail Distribution County Administrator

Louisa County

Michael Crist P.O. Box 160

Plant Manager Louisa, VA 23093

North Anna Power Station

Virginia Electric & Power Company

Electronic Mail Distribution

Lillian M. Cuoco, Esq.

Senior Counsel

Dominion Resources Services, Inc.

Electronic Mail Distribution

Tom Huber

Director, Nuclear Licensing & Operations

Support

Virginia Electric and Power Company

Electronic Mail Distribution

Ginger L. Rutherford

Virginia Electric and Power Company

Electronic Mail Distribution

Virginia State Corporation Commission

Division of Energy Regulation

P.O. Box 1197

Richmond, VA 23209

Attorney General

Supreme Court Building

900 East Main Street

Richmond, VA 23219

Senior Resident Inspector

North Anna Power Station

U.S. Nuclear Regulatory Commission

P.O. Box 490

Mineral, VA 23117

VEPCO 4

Letter to David A. Heacock from Victor M. McCree dated October 31, 2011

SUBJECT: NORTH ANNA POWER STATION - AUGMENTED INSPECTION TEAM (AIT)

REPORT 05000338/2011011, 05000339/2011011, 07200016/2011001, and

07200056/2011002

Distribution w/encl:

C. Evans, RII EICS

L. Douglas, RII EICS

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMNorthAnna Resource

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-338, 50-339, 72-16, 72-56

License Nos.: NPF-4, NPF-7, SNM-2507, COC-1004

Report No.: 05000338/2011011, 05000339/2011011, 07200016/2011001 and

07200056/2011002

Licensee: Virginia Electric and Power Company (VEPCO)

Facility: North Anna Power Station, Units 1 & 2 and the North Anna Independent

Spent Fuel Storage Installation

Location: 1022 Haley Drive

Mineral, Virginia 23117

Dates: August 30, 2011 through October 3, 2011

Team Leader: M. Franke, Chief

Operations Branch 2

Division of Reactor Safety

Assistant Team G. Kolcum, Senior Resident Inspector, North Anna

Leader:

Inspectors: R. Jackson, Senior Resident Inspector, Construction Projects Branch 4,

Division of Construction Projects

S. Walker, Senior Reactor Inspector, Engineering Branch 1,

Division of Reactor Safety

L. Suggs, Reactor Inspector, Engineering Branch 2,

Division of Reactor Safety

Y. Li, Senior Geophysicist (Seismologist), Mechanical and Civil

Engineering Branch

Office of Nuclear Reactor Regulation

M. Chakravorty, Senior Structural Engineer, Structural Engineering

Branch 2

Office of New Reactors

S. Park, Structural Engineer, Structural Engineering Branch 1

Office of New Reactors

Approved by: Victor M. McCree, Regional Administrator

Enclosure

TABLE OF CONTENTS

Contents

1.0 Executive Summary ........................................................................................................ 2

2.0 Description of Event ........................................................................................................ 3

2.1 Summary Sequence ............................................................................................ 3

2.2 System Descriptions ............................................................................................ 4

3.0 Seismic Assessment ....................................................................................................... 6

3.1 Seismic Strength ................................................................................................. 6

3.2 Seismic Equipment Maintenance and Calibration .............................................. 19

4.0 Cause of Unit 1 and Unit 2 Reactor Trip ........................................................................ 21

5.0 Emergency Diesel Generator Performance ................................................................... 22

6.0 Electrical System Performance ..................................................................................... 27

7.0 On-Shift Human Performance ....................................................................................... 37

7.1 Emergency Operating Procedures (EOPs) ........................................................ 37

7.2 Station Black-Out Diesel Generator ................................................................... 39

7.3 2H Emergency Diesel Generator Failure ........................................................... 40

7.4 Restoration of Offsite Power .............................................................................. 41

7.5 Emergency Planning Declarations ..................................................................... 41

7.6 Post Earthquake Actions ................................................................................... 43

8.0 Plant Parameters and Assessment ............................................................................... 45

8.1 Unexplained Instrumentation Anomalies............................................................ 45

8.2 General Assessment ......................................................................................... 46

8.3 Groundwater and Buried Pipe ........................................................................... 51

9.0 Operability Determinations ............................................................................................ 52

10.0 Restart Readiness ........................................................................................................ 56

11.0 Independent Spent Fuel Storage Installation (ISFSI)..................................................... 57

12.0 Data for Risk Assessment ............................................................................................. 59

13.0 Safety Culture ............................................................................................................... 60

14.0 Exit Meeting Summary .................................................................................................. 61

ATTACHMENT 1 - Supplemental Information

ATTACHMENT 2 - Sequence of Events

ATTACHMENT 3 - Augmented Inspection Team Charter

ATTACHMENT 4 - Public Exit Meeting Slides

SUMMARY OF FINDINGS

IR 05000280/2011011 and 05000281/2011022; IR 07200016/2011001 and 07200056/2011002,

08/30/2011 through 10/03/2011, North Anna Power Station, Units 1 and 2; Augmented

Inspection Team.

An Augmented Inspection Team (AIT) was dispatched to the site on August 30, 2011, to assess

the facts and circumstances surrounding an earthquake event, dual unit trip, and loss of offsite

power that occurred on August 23, 2011. The AIT was established in accordance with NRC

Management Directive 8.3, NRC Incident Investigation Program, and implemented using

Inspection Procedure 93800, Augmented Inspection Team.

The inspection was conducted by a team of inspectors from the NRCs Region II office, senior

resident inspectors from North Anna and Construction Projects Branch 4, one Seismologist from

the NRC Office of Nuclear Reactor Regulation (NRR), and two Structural Engineers from the

NRC Office of New Reactors (NRO.) The team identified 7 issues that will require additional

NRC inspection. These issues are tracked as unresolved items in this report.

A. NRC-Identified and Self-Revealing Findings

None

B. Licensee-Identified Violations

None

Enclosure

2

1.0 Executive Summary

On August 23, at about 1:51 p.m. Eastern Daylight Time (EDT), North Anna Power Station

experienced a magnitude 5.8 earthquake with an epicenter about twelve miles southwest of the

plant. Both reactors experienced automatic trips from 100 percent power. Offsite electrical

power to the site was interrupted. All four emergency diesel generators automatically started,

loaded and provided power to the emergency buses. All control rods inserted into the core. An

Alert was declared based on shift managers judgment.

At about 2:40 p.m., control room operators stopped the 2H emergency diesel generator (EDG)

after a cooling water leak and rising temperatures were observed on the diesel engine.

Operators subsequently aligned the stations blackout (SBO) diesel generator (DG) to power the

2H vital bus. At 5:40 p.m., offsite power was first restored to the 2J emergency bus via the C

reserve station transformer. Offsite power to the site was fully restored to the emergency

busses by 10:58 p.m., and both units were later brought to cold shutdown for further inspection

and repairs.

Because it was unclear whether the ground motion from the earthquake had exceeded the

plants licensed design basis, and because of potential safety ramifications, the NRC dispatched

an Augmented Inspection Team to better understand the event and the licensees response.

The teams findings included: (1) operators responded to the event in accordance with

established procedures and in a manner that protected public health and safety; (2) the ground

motion from the earthquake exceeded the plants licensed design basis; (3) no significant

damage to the plant was identified; (4) safety system functions were maintained; and (5) some

equipment issues were experienced.

The team evaluated the event to determine if any issues should be considered on a generic

basis for other facilities. The team identified two potential issues in the areas of (1) seismic

monitoring instrument location, and (2) seismic monitoring equipment performance.

The team identified several specific issues related to equipment performance that warranted

follow-up. These included: (1) the 2H EDG developed a cooling water leak necessitating its

shutdown; (2) operators observed frequency oscillations affecting the 1J EDG that appeared to

approach Technical Specification (TS) limits; (3) some functions of the control room seismic

alarm panel were lost during the earthquake; (4) seismic instrumentation, data collection and

operator training issues were revealed; (5) missing cooling water orifice plates were identified

on the 1J and 2J EDGs; (6) an Auxiliary Feedwater Pump (AFWP) trouble alarm was

unexpected during the event; and (7) some anomalies were observed affecting some safety

related instrumentation during the event. These issues are documented as unresolved items in

this report.

Overall, the team concluded that the event did not adversely impact the health and safety of the

public. Safety limits were not approached and there was no measurable release of radioactivity

associated with the event.

Enclosure

3

2.0 Description of Event

2.1 Summary Sequence

Before the event, the North Anna electrical distribution system was in an at power

configuration and the 4160 volt portion of the system was aligned with Buses D, E, and F

powering the emergency buses from Units Reserve Station Service Transformers

(RSST). Figure 1 below shows a simplified schematic of the North Anna electrical

distribution system. This figure, along with the system descriptions in Section 2.2 of this

report, will aid in understanding the details of this event. Both Units were at 100% power

and Unit 1 turbine driven AFWP was removed from service for scheduled surveillance

testing.

Figure 1, North Anna Simplified Electrical Distribution

On August 23, 2011, at approximately 1:51 p.m. EDT, the site experienced a magnitude

5.8 earthquake with an epicenter approximately twelve miles southwest of the plant.

Both reactor trip breakers opened on negative flux rate approximately 11 seconds after

the event. Sudden pressure relay actuations were experienced on the RSSTs

approximately 12 seconds after the event, leading to a loss of off-site power (LOOP)

event. At approximately 20 seconds after the event, all four EDGs and the SBO DG

Enclosure

4

auto started. An Alert was declared at 2:03 p.m. based on shift managers judgment due

to an inability to enter the emergency action level (EAL) for a seismic event because the

LOOP prevented the seismic panel from reporting the earthquake magnitude in the

control room. At 2:40 p.m., 2H EDG was tripped in the control room due to a coolant

leak. At 2:55 p.m., an Alert was declared for Unit 2 due to the loss of 2H EDG.

Approximately 38 minutes later, the SBO DG was aligned to the 2H bus. At 10:58 p.m.,

offsite power was restored supplying all the emergency buses. Both units were safely

shutdown and stabilized under hot shutdown conditions.

A more detailed sequence of events can be found in Attachment 2.

2.2 System Descriptions

2.2.1 Emergency Diesel Generators

There are two 100 percent capacity EDGs for each unit. The EDGs automatically start

when a safety injection signal is received, a 90 percent degraded voltage level for 56

seconds is sensed on the bus, or about 74 percent voltage for 2 seconds exists on the

bus. Following a LOOP, as experienced on August 23, 2011, when the EDGs sense

voltage less than 74 percent on the bus, the emergency bus isolates and load shedding

begins. The generator output breaker automatically closes onto the bus when the

generator output voltage reaches 95 percent of nominal, either of the normal offsite

power supply breakers are open, limited residual voltage remains on the bus, and the

generator differential auxiliary relay is reset.

The EDG supply breaker automatic protective trips are diesel-engine overspeed,

generator overexcitation, bus overcurrent, and generator differential. The EDG

automatic engine trips are high lube-oil temperature, high jacket water coolant

temperature, high crankcase pressure, low lube-oil pressure, start failure, generator

differential, and diesel-engine overspeed. During an emergency start, the EDG breaker

trips automatically only on diesel overspeed, bus overcurrent, and generator differential.

The EDGs are automatically shut down only on generator differential and diesel-engine

overspeed. All other EDG protective trips are bypassed during an emergency start. The

breakers can also be manually tripped, and the diesels manually stopped.

The EDG jacket water cooling system is designed to dissipate the heat rejected by the

engine water jackets and the lube oil. Coolant is circulated through the engine at about

800 gpm by an engine driven centrifugal pump. It then passes through a temperature

control valve which directs it through or around the radiator as necessary to maintain

required temperature. Then the coolant passes through the lube oil heat exchanger

where it enters the pump suction and repeats the cycle. If jacket coolant is lost, there is

a high jacket coolant temperature alarm. The trip setpoint of 205°F is 111% of normal

operating temperature, which is low enough to protect the engine but high enough to

prevent inadvertent tripping. The alarm setpoint is 195°F.

The EDGs are load tested in accordance with TS. To allow isochronous (independent)

and droop (parallel) operation of the EDG following testing, an automatic speed reset

Enclosure

5

capability has been installed in the EDG motor-operated potentiometer circuit. The

preset speed condition (900 rpm) is necessary for two reasons: (1) to ensure that the

EDGs can accommodate the oncoming load without tripping, and (2) to ensure that

control instrumentation and other safety-related equipment will operate at the proper

frequency. Following the shutdown of the EDG system, the reset will automatically

position the speed reference potentiometer to the predetermined speed setting on the

electric governor. The control relays that are used for this purpose are powered from the

125V DC distribution panels 2A and 2B.

2.2.2 Electrical Power Distribution System

The onsite electric system includes electrical equipment necessary to generate power

and deliver it to the high-voltage switchyard. It also includes power supplies and

equipment, including batteries, necessary to distribute power, both AC and DC, to the

normal (non-safety-related) auxiliaries, and emergency (safety-related) auxiliaries. The

onsite electric system also supplies power for control and instrumentation and is

designed to provide dependable sources of power and distribute it to the plant

auxiliaries.

The normal AC power source for each unit is the main generator, which is connected to

three unit station service transformers by the isolated phase bus duct. The transformers

have adequate capacity to supply all unit auxiliaries, with the exception of 4-kV buses

1G and 2G, for plant operation during normal power generation. Buses 1G and 2G are

powered from the offsite sources via the Reserve Station Service Transformers (RSSTs)

B and C, respectively.

The preferred or reserve AC power source is the switchyard, which is connected to both

units via three 3-phase 34.5/4.16-kV transformers located near the power station. The

34.5-kV supply to these RSSTs comes from two or more of the following: two 500/36.5-

kV transformers located in the 500-kV switchyard, and one 230/34.5-kv transformer

located in the 230-kV switchyard. A switching capability is provided so that all three of

the 34.5/4.16-kV transformers can be supplied from any of the station reserve

transformers if necessary. The reserve station service power is available at all times to

the safety-related equipment and has the capacity to power the station auxiliaries in the

event of a loss of the normal AC power supply. Upon a loss of power from the normal

source on Unit 2, the normal station distribution system will transfer automatically to the

reserve station service supply, provided no fault exists on the normal 4160V bus. On

Unit 1, a main generator breaker has been installed. This allows Unit 1 to have its

normal station service buses supplied from its normal station service transformers

(backfed from the 500-kV switchyard) for most Unit 1 trips.

The standby emergency AC power source for each unit consists of two EDGs. The

standby AC power system has adequate capacity to supply the safety-related

equipment. The standby AC power source, during the periods of interrupted preferred

power, automatically supplies safety-related equipment.

Enclosure

6

An Alternate AC (AAC) DG is available to provide emergency power in the event of a

SBO. A SBO is defined as loss of offsite power, concurrent with a turbine trip (loss of

onsite power) and the failure of the emergency AC power source, but not the station

batteries for the blacked out unit. The AAC system is auto-started by an SBO event.

Operator action is required to align the AAC DG output to the desired emergency bus.

The 120V vital AC power source consists of four static inverters, each powered from its

associated DC bus. These inverters provide a dependable 120V AC power source for

the safety-related equipment, control, and instrumentation.

The 125V DC power source in each unit consists of four independent batteries and six

battery chargers, two of which are spares.

The onsite AC power distribution system consists of three normal 4160V buses, two

emergency 4160V alternate AC buses, two emergency 4160V buses per unit, and four

emergency 480V buses per unit. In addition, Unit 1 is equipped with 11 normal 480V

buses and Unit 2 is equipped with eight normal 480V buses. The 480V buses are fed

from their respective 4160V buses through transformers. The 480V buses feed motors,

motor control centers, transformers for 240/120V AC power and lighting distribution, and

battery chargers for the 125V DC system and the standby diesel generators 125V DC

systems.

3.0 Seismic Assessment

The team collected data to determine the strength of the seismic activity at the plant.

This included information about the maintenance and calibration of seismic monitoring

equipment installed at the plant.

3.1 Seismic Strength

a. Inspection Scope

The scope of the task was to determine the seismic impact at the North Anna Nuclear

Power Station from the August 23, 2011, earthquake. In order to complete the task, the

team reviewed seismic recordings and associated response spectra from seismic

monitors situated at different levels of the Unit 1 containment and Auxiliary Buildings.

The team performed a walkdown of different levels of the Auxiliary Building and the Unit

1 Containment Building where seismometers were located. In addition, the team

interviewed licensee engineers.

Enclosure

7

b. Observations and Findings

The team found that the ground motion from the earthquake exceeded the licensees

design basis.

The seismic vibratory effect to the reactor and its associated structures, systems and

components was directly demonstrated by comparing the design spectrum with

seismometer recordings at the same elevation. The Seismic Monitoring Equipment table

following this section lists elevations, structure, or system, affiliations and equipment

types for seismometers inside two buildings as well as a synopsis of the comparison

between the design and the observed spectrum. In addition, Figures 1-10 show a

comparison between the design response spectrum and the seismic recordings,

corresponding to the tables description.

The design response spectrum was exceeded based on recordings from different types

of seismic instruments. This was evident on both of the seismic recording systems,

Kinemetrics accelerometers and Engdahl scratch plates, used at the plant. However,

recordings from the two different seismic instruments (Kinemetrics and Engdahl) located

at the same floor level show conflicting spectral behaviors in terms of both frequency

and amplitudes. The team relied primarily on the information obtained from the

Kinemetrics equipment because Engdahl scratch plates only record certain maximum

levels as opposed to recording the entire time history of the event; and in this case some

of the scratch plates did not register any of the seismic event activity. Additional

discussion of the seismic instrumentation performance can be found in Section 3.2.

As part of the seismic system assessment, the team walked down the Auxiliary Building

and the Unit 1 Containment Building to visually inspect various structures, systems and

components as well as seismic instruments located at different floors. The walkdown

included a majority of the Unit 1 Containment Building and Auxiliary Building elevations.

During the walkdowns, the team did not observe significant damage. The team observed

some minor cracks in the interior wall of the Auxiliary Building and a minor crack on the

inCore room wall inside the Unit 1 Containment Building. During interviews, licensee

personnel indicated that no soil failure, neither liquefaction nor slope failure, were

observed at the North Anna site.

Enclosure

8

Seismic Monitoring Equipment

Structures Elevation Description Frequency Largest Other Seismometers

(Seismometer) And sensitive to difference (%)

Direction SSC) and associated

frequencies

Unit 1 Basemat Recorded ground Exceeded 100% at Engdahl scratch plate recordings

(Kinemetrics 216 ft motion exceeded from 2.5 Hz approximately exist; no exceedance at all

SMA-3) in the N-S DBE (5% damping) and above, 40 Hz and recorded frequencies but no

Figure 1 except at 8 above readings at 10.1 and 25.4 Hz, and

Hz conflict with Kinemetrics SMA-3

recordings

Unit 1 Basemat Recorded ground Exceeded at 31% at about 30 Engdahl scratch plates recordings

(Kinemetrics) 216 ft motion exceeded several Hz with minor exceedance at 2,8,

Figure 1 in the E-W DBE (5% damping) frequency 12.7 , 16 and 25.4 Hz only

bands

centered at

12, 16 and

30 Hz

Unit 1 Basemat Recorded ground Exceeded 88% at 29 Hz Engdahl scratch plates recordings

(Kinemetrics) 216 ft motion exceeded from 3 Hz with exceedance at 10.1 and 25.4

Figure 2 in the DBE (5% damping) and above Hz only

Vertical

Unit 1 Elevation Recorded ground Exceedance 74% at 3 Hz No Engdahl data available

(Kinemetrics) 291 ft motion exceeded almost

Figure 3 in the N-S DBE (5% damping) continuously

from 1 to 3

Hz and 7.8

Hz and

above

Unit 1 Elevation No exceedance at all No Engdahl data available

(Kinemetrics) 291 ft the frequencies

Figure 3 in the E-W

Unit 1 Elevation Recorded ground Exceeded at 176 % at about No Engdahl data available

(Kinemetrics) 291 ft motion exceeded 3-4 Hz, 5-10 40 Hz

Figure 4 in the DBE (5% damping) Hz and 26

vertical Hz and

above

Auxiliary Basemat Recorded ground Exceeded 83% at 10 Hz No Kinemetrics data available

Building 241ft motion exceeded between 6.4

(Engdahl in the N-S DBE (2% damping) Hz and 22

Scratch plates) Hz

Figure 5

Auxiliary Basemat No exceedance at all No Kinemetrics data available

Building 241ft the frequencies

Figure 6 in the E-W

Auxiliary Basemat Recorded ground Exceeded at Approximately No Kinemetrics data available

Building 241ft motion exceeded 6.4 Hz and 200% at 25.4 Hz

Figure 7 In the DBE (2% damping) above

vertical

Auxiliary Elevation Recorded ground Exceeded at Approximately No Kinemetrics data available

Building 273 ft motion exceeded 5.3 Hz and 450% at 12.7 Hz

Figure 8 in the N-S DBE (2% damping) above

Auxiliary Elevation Recorded ground Exceeded at Approximately No Kinemetrics data available

Building 273 ft motion exceeded 8 Hz and 23 200% at 20.2 Hz

Figure 9 in the E-W DBE (2% damping) Hz

Auxiliary Elevation Recorded ground Exceeded at Approximately No Kinemetrics data available

Building 273 ft motion exceeded 6.4 Hz and 250% at 10 Hz

Figure 10 in the DBE (2% damping) above

vertical

Enclosure

9

1.2

1

0.8

acceleration (g)

0.6

SSE (horizontal)

Observed (NS)

0.4

Observed (EW)

0.2

0

0.1 1 10 100

Frequency (Hz)

Figure 1, Unit 1 basemat spectrum comparison (horizontal) between the designed and the

observed

Enclosure

10

0.4

0.35

0.3

0.25

Acceleration (g)

0.2 OBE (vertical)

SSE (vertical)

Observed (vertical)

0.15

0.1

0.05

0

0.1 1 10 100

Frequency (Hz)

Figure 2, Unit 1 basemat spectrum comparison (vertical) between the designed and the

observed

Enclosure

11

ectrum comparison (horizontal) between the desig

Figure 3, Unit 1 Operating Deck spe gned and

the observed

Enclosure

12

ectrum comparison (vertical) between the designe

Figure 4, Unit 1 Operating Deck spe ed and the

observed

Enclosure

13

Figure 5, Auxiliary Building basemat spectrum comparison (N-S) between the designed and the

observed

Enclosure

14

Figure 6, Auxiliary Building basemat spectrum comparison (east-west) between the designed

and the observed

Enclosure

15

Figure 7, Auxiliary Building basemat spectrum comparison (vertical) between the designed and

the observed

Enclosure

16

Figure 8, Auxiliary Building (273 ft) spectrum comparison (north-south) between the designed

and the observed

Enclosure

17

Figure 9, Auxiliary Building (273 ft) spectrum comparison (east-west) between the designed and

the observed

Enclosure

18

Figure 10, Auxiliary Building (273 ft) spectrum comparison (vertical) between the designed and

the observed

Enclosure

19

3.2 Seismic Equipment Maintenance and Calibration

a. Inspection Scope

The team reviewed records and interviewed personnel to determine whether the seismic

instruments at the North Anna Power Station were maintained and calibrated properly to

provide accurate information for making decisions on safe shutdown during and

following a seismic event and for subsequent engineering analysis. The team completed

this task by reviewing seismic instrument manuals, and other related documents, and a

sample of calibration documents. The team also interviewed licensee engineers and

inspected instrument scratch plates that recorded the initial seismic activity.

b. Observations and Findings

The team found that two potential generic issues exist related to the seismic

instrumentation system and implementation. These issues and one related URI are

described in this section. A second related URI is described in Section 7.5.

The team conducted walkdowns of all seismic instruments located in Unit 1 Containment

and Auxiliary Buildings. During the walkdowns, the team visually inspected all of the

seismic instruments at various levels of elevation of the two buildings. The installation of

seismic equipment appeared consistent with the equipment vendor manuals. The

licensees records indicated that seismic equipment, including both Engdahl and

Kinemetrics, was checked every 18 months during refueling outages.

Through review of records and interviews with licensee personnel, the team noted the

following issues with seismic instruments:

1. All the seismic instrumentation was located on plant structures, and no

seismometers were installed on a free surface in the free field; therefore, the team

questioned whether the instrumentation would provide a reliable indicator for

determining whether an earthquake had exceeded Operating Basis Earthquake

(OBE) or Safe Shutdown Earthquake (SSE) ground motion levels.

2. A seismic alarming system panel lost power during the event and it was not

connected to an uninterruptible electric power supply. In addition, some other

equipment issues were observed during the event follow-up. The team questioned

whether the seismic equipment and associated alarming systems were adequate to

perform their expected function considering the equipment issues observed during

the event.

Because these two issues may be applicable to other operating nuclear power plants,

the team determined that they represented potential generic issues.

Enclosure

20

Specific issues with the equipment included:

  • A seismic alarming system panel lost power during the event and it was not

connected to an uninterruptible electric power supply. The team questioned whether

the seismic equipment and associated alarming systems were adequate to perform

their expected function considering equipment issues observed during the event.

  • Seismic recordings were inconsistent between the Kinemetrics and Engdahl scratch

plates located on the base-mat of Unit 1. Some of the Engdahl scratch plates did not

record any ground motion.

  • Both orientations of Kinemetrics and Engdahl scratch plate equipment located at

different elevation levels were misidentified; therefore, the data for East-West and

North-South was initially swapped.

  • A deficiency was previously identified by the licensee on the seismic alarming

system, affecting one of the panels alarms, but remained pending repair (Work

Order 59102235553 and Condition Report (CR) 403883).

  • Instrument Panel OBE and SSE values were not consistent with FSAR 3.7.4 (OBE

exceedance) and the licensees system training manual (Module NCRODP-72-NA:

amber light indicates 67 percent of DBE for frequency of a particular reed in either

the L, T or V direction; red light indicates 100% DBE for the frequency of a particular

reed in either the L,T or V direction). The licensee entered this issue into their

corrective action program as CR 442880.

  • Based on the review of maintenance and calibration records, the team did not find

documentation indicating performance of cross-checks and calibration of different

types of seismic equipment against each other to ensure the signals recorded were

consistent with regard to frequency and amplitudes.

  • Seismic recordings were not clocked or referenced to the plants event recorders;

therefore, the start time of seismic activity time history recordings required

estimation.

The team determined that the issues with seismic instrument implementation warranted

additional NRC review and follow-up considering that information from this system

served as an input into event response decision making. Additional review by the NRC

will be needed to determine whether any of the issues represents a performance

deficiency. An unresolved item will be opened pending completion of this review. The

issue will be identified as URI 05000338, 339/2011011-01, Seismic Instrumentation

Implementation.

Enclosure

21

4.0 Cause of Unit 1 and Unit 2 Reactor Trip

a. Inspection Scope

To ascertain what caused the reactor trip on August 23, 2011, the team conducted

interviews with licensee staff to gather an accurate account of the sequence of events.

Plant data and logs were reviewed to gain an understanding of plant response. The

Post Trip Event Report was reviewed to gauge the licensees assessment of the plant

trip and the identified possible causes.

b. Observations and Findings

Based on the sequence of events, the team found that the reactor trips resulted from

high negative rate flux signals and occurred prior to the loss of offsite power.

Based on the plant response data, the licensee determined that both Unit 1 and 2

reactor trips were due to a Power Range High Negative Neutron Flux Rate reactor trip

signal. The bi-stables (N41 and N42) associated with the high negative flux rate trip are

for an abnormal rate of decrease in nuclear power. The reactor is tripped when a high

negative rate occurs in two out of the four power range channels. The licensees Post

Event Trip Report identified four possible causes for this trip:

  • Movement of the nuclear instrumentation detectors
  • Core barrel movement

At the time of the teams review, the licensee was conducting a root cause evaluation

and planned to assess each one of these potential causes through engineering analysis

and testing to determine the most likely underlying cause of the trip signal and any

contributing causes. The licensee had not yet completed their root cause at the time of

the inspection.

Enclosure

22

5.0 Emergency Diesel Generator Performance

a. Inspection Scope

To adequately evaluate the performance of the EDGs in response to the seismically

induced LOOP (including the 2H EDG coolant leak and any identified anomalies), the

team performed the following activities:

  • Conducted walkdowns of the EDGs to evaluate the material condition
  • Conducted interviews with plant personnel (maintenance, engineering, and

operations; root cause investigation team) to determine an accurate account of

events related to the EDGs

  • Reviewed design and engineering documents to verify appropriateness of licensee

actions in accordance with design and licensing basis

  • Observed corrective maintenance and testing to assess the licensees actions to

restore the EDGs

In addition, the team reviewed corrective action CRs to evaluate the licensees response

to identified deficiencies associated with the EDGs. The vendor manual was referenced

to verify alignment with licensee maintenance procedures. Industry operating

experience was referenced to identify any potential generic industry issues similar to

what was observed at North Anna with respect to the EDGs performance.

b. Observations and Findings

The team found some issues with EDG performance and identified two URIs that are

described in this section.

Following the seismic event on August 23, 2011, at 1:51 p.m., all four EDGs started and

loaded their respective emergency buses due to a loss of offsite power on both units.

About 45 minutes after the EDGs started, a coolant leak was observed on the 2H EDG.

At 1:40 p.m., the 2H EDG was manually tripped and secured and the associated

emergency bus de-energized. The 2H emergency bus was subsequently re-energized

by the SBO diesel. Additionally, the 1J EDG was observed to have minor frequency

oscillations. This issue is discussed in further detail in Section 6.0 of this report.

Upon further investigation, it was determined that the 2H EDG coolant leak was caused

by failure of a fiber gasket located between the exhaust belt and the jacket water cooling

inlet jumper on the opposite control side (OCS) of the diesel engine. Initial discovery

found the gasket soft and extruding from the flange edge. Due to the excessive coolant

leak and in response to a High Jacket Coolant Temperature annunciator that came in

during the event, the licensee inspected the cylinder liners, pistons, and rings for

damage. No engine damage was found to have occurred. During restoration of the 2H

EDG, a small exhaust leak was also identified during the post-maintenance test. The

licensee subsequently replaced one exhaust gasket and the extension pipe. The small

leak did not have an impact on the EDG to perform its safety function.

Enclosure

23

2H EDG Jacket Water Cooling Gasket Leak

In May 1999, EDG vendor Fairbanks-Morse issued a Marketing Information Letter,

Vendor Technical Manual (VTM) Addenda 72, detailing a new, fiber gasket to replace

the previous rubber gaskets for the cooling water bypass fittings. The licensee began

installation of the new gaskets in 2001. One major difference was the new fiber gasket

was 1/8 thick as opposed to 1/16 for the rubber gasket. The letter also provided

recommendations for gasket installation. These recommendations included:

  • Allowing a minimum dry time of 10 minutes following application of the gasket

adhesive;

  • Ensure the fitting surfaces for the exhaust belt and the water inlet flange have the

appropriate finish;

  • Assemble fitting to exhaust belt and torque nuts to 70 ft/lbs +/- 10

Maintenance procedure, 0-MCM-0701-27, Replacement of Emergency Diesel Generator

Cylinder Liners, Revision 19, was used for replacement of the gaskets on 2H EDG in

May 2010. The procedure did not include a dry time following application of the

adhesive (RTV). Improper curing time for the adhesive could impact the proper

alignment of the gasket; too short a time can allow the gasket to move out of place, too

much time can harden the adhesive. Following overhaul of the 2H EDG in May 2010,

which included replacement of the gaskets, the licensee performed a hydrostatic test to

ensure proper restoration. During this test, water pressure was applied (at approx. 50

psi) to the engine block above the normal operating pressure (approx. 30 psi) to ensure

no external leakage was occurring; however, coolant leakage was observed on all of the

gaskets. It was determined at this time, as documented in Condition Report (CR)

383161 and Corrective Action (CA) 172549, that the RTV adhesive should be allowed to

set for 30 - 60 minutes on the gaskets prior to installation for improved sealing. The 2H

EDG gaskets were removed and re-installed and passed a subsequent hydrostatic post-

maintenance test. A subsequent revision to the procedure was approved and

implemented in September 2010 to include the adhesive cure time.

When the 2H EDG was taken out of service for corrective maintenance following

discovery of the coolant leak on August 23, 2011, the licensee removed the OCS heat

shields and stress bars, drained the remainder of the coolant, and removed the exhaust

components as necessary to gain access to the jacket water inlet elbow. Initial

inspection of the water by-pass inlet revealed the gasket protruding past the inlet fitting

indicating that the gasket might not have been properly aligned when originally installed

in May 2010, despite having been installed twice and satisfactory completion of the

hydrostatic testing. Additional investigation by the licensee revealed that in addition to

potential misalignment of the water bypass inlet gasket, the jacket water bypass inlet

header adjustable screw and jam nut were potentially inappropriately installed. The

adjustable screw and jam nut act as a cantilever on the engine block and bypass inlet

fittings. Excessive tightening of the adjusting screw can place more compression on the

top of the gasket and cause the gasket to extrude and leak on the bottom of the inlet

pipe joint. There was no guidance in procedure 0-MCM-0701-27 for tightening the

Enclosure

24

adjustment screw and jam nut; the procedure has since been revised to include detailed

instructions.

Figure 11, 2H EDG Failed Gasket

Following installation of the gaskets in May 2010, 0-MCM-0701-27 required the water

bypass fitting bolts be torqued to 50 -55 ft-lb; however, this was in conflict with the

vendor recommended 70 ft-lbs. as outlined in VTM Addenda 72. According to the

vendor, the 50 ft-lb torque specification was applicable to the previous rubber gasket and

was specified to reduce the thickness of the gasket from 1/16 (.062) to .040-.050. The

new gasket was thicker at 1/8 and the 70 ft-lbs. was the specified torque. There are two

bolts per fitting and are torqued to ensure appropriate compression was applied between

the bypass fitting, the gasket, and the exhaust belt. This discrepancy in torque values

was identified by the licensee and documented in CR 347658 in September 2009. After

discussion with the EDG vendor, the licensee determined that the lower torque value

was acceptable given no leakage up to that time had been observed during hydrostatic

testing or operation of the diesel; however, the vendor maintained a recommendation of

70 ft-lbs. if leakage was observed. In response to the 2H EDG coolant leak on August

23, 2011, the licensee conducted follow-up discussions with the vendor to determine if

50 ft-lbs. was acceptable. The vendor restated the recommendation of 70 ft-lbs. and

performance of a hydrostatic test at 50 psi. The team questioned whether the lower 50

ft-lbs. torque value being applied to the new thicker gasket provided the appropriate

compression for sealing. A lack of compression can allow the gasket to absorb water

and soften, which can lead to gasket extrusion from the flange edge. The licensee was

going to perform a technical evaluation to demonstrate adequate compression was

available to the gasket. The procedure has since been revised to include the

recommended 70 ft-lbs. torque specification.

Enclosure

25

Additionally, in September 2009, the licensee documented in CR 347783 that the EDG

water bypass fittings had the incorrect surface finish and were not in accordance with the

VTM Addenda 72 recommendation of ensuring the exhaust belt had a 125 micro-inch

finish and the inlet flange had a 250 micro-inch finish. Though the CR was written to

resolve the discrepancy before the next EDG outage (1J), the procedure was not revised

until August 2011, following the 2H EDG coolant leak.

The team concluded the licensee failed to properly incorporate or evaluate vendor

recommendations regarding installation of the cooling water gaskets. At the time of the

teams review, the licensee planned to continue evaluating whether the seismic event

accelerated the failure of the gasket. Though the licensee eventually inspected all four

EDGs following the discovery of the leak on 2H EDG, the team questioned why the

licensee initially determined the leak to be an isolated event without having known the

cause. The TS requires a common cause evaluation if one EDG is determined to be

inoperable. If the cause cannot be confirmed not to exist on the remaining EDGs, the

EDGs should be tested to provide reasonable assurance and the corrective action

program should continue to evaluate the common cause possibility for the other EDGs.

In the case of the 2H EDG leak, the apparent cause was known to be the gasket failure

as documented in CR 439091 on August 24, 2011. At the time, the other EDGs were

running at full load to support plant shutdown; however, it was not known if the gaskets

were installed properly on these EDGs. The CR recognized that previous related issues

existed (i.e., multiple coolant leaks across multiple EDGs); however, the licensee still

determined the leak was an isolated event. The team observed that this conclusion was

based on lack of visible evidence or result (i.e., coolant leakage), but not on a

determination of the actual cause. The licensee did submit work orders to inspect the

gaskets on the remaining EDGs, but the initial assessment of this being an isolated

event did not appear in accordance with proper corrective action program common

cause evaluations.

The failure of the jacket water cooling gasket caused a leak on the 2H EDG and

consequently, inoperability of the 2H EDG during a dual unit LOOP following a seismic

event on August 23, 2011. Additional review by the NRC will be needed to determine

whether the lack of adequate procedural guidance for EDG cooling water gasket

installation represents a performance deficiency. An unresolved item will be opened

pending completion of this review. The issue will be identified as unresolved item (URI)

05000338, 339/2011011-02: Failure of 2H Emergency Diesel Generator Jacket Water

Cooling Gasket Resulting in Inoperability During Dual Unit LOOP.

1J & 2J EDG Jacket Water Cooling Pumps Missing Orifice Plate

Following the seismic event on August 23, 2011, and subsequent failure of the 2H EDG,

all four EDGS were subject to thorough inspection and corrective maintenance. On

September 3, 2011 during a post-maintenance EDG run, a leak was observed on 1J

EDG engine-driven jacket coolant water pump. When the pump was removed for

rebuild, it was discovered the pump did not have an orifice plate installed on the

discharge of the pump. The orifice plate was subsequently found still attached to the

discharge flange of the previously removed pump. An extent of condition was performed

Enclosure

26

and it was observed that the 2J EDG was also missing its orifice plate on the jacket

cooling water pump.

A missing orifice plate on the jacket cooling water pump discharge flange can cause

increased flow and pressure in the jacket cooling system, which in turn can cause 1)

operating pressures to reach limitations; (2) degraded cooling capabilities; and (3)

potential pipe strain that could lead to leakage or pump and piping fatigue. An installed

orifice plate creates a pressure drop and corresponding decrease in flow throughout the

system. As flow decreases, the temperature delta must increase to maintain the same

amount of heat removal. It was determined the 2J EDG was missing its orifice plate

since the last time it was worked on in 2004. A review of past performance data for the

2J EDG (back to 2005) was conducted and it was observed that due to the increased

parameters, the temperature delta is lower at full load than normally (4-5 deg. vs. 10-14

delta T normally). Additionally, the 2J engine has required more work input from the

engine which lowered the available horsepower to turn the electrical generator; however,

past surveillance testing has demonstrated the ability of the 2J EDG to reach rated load.

Because the degraded 2J EDG engine driven coolant pump caused some parameter

changes on the 2J EDG and could have caused some degradation to the diesel since

2004, additional review by the NRC will be needed to determine whether the missing

orifice plate represents a performance deficiency. An unresolved item will be opened

pending completion of this review. The issue will be identified as URI 05000338,

339/2011011-03: Missing Orifice Plate on 1J and 2J EDG.

Enclosure

27

6.0 Electrical System Performance

a. Inspection Scope

The team performed the following actions to evaluate the performance of the electrical

system of the station:

The team evaluated the electrical perturbations at the site during and subsequent to the

earthquake, and until offsite power was restored to all emergency buses:

  • Reviewed CRs generated during and subsequent to the seismic event pertaining to

electrical perturbations or anomalies, equipment failures and spurious equipment

actuations.

  • Conducted independent visual inspections and walkdowns of a sample of safety

related 4160V load centers, 480V motor control centers (MCCs), inverters, batteries,

and battery chargers on both units to assess the general condition of systems and

components to determine whether there was visible evidence of damage or

significant movement as a result of seismic activity

  • Observed licensee staff during electrical system walkdowns to examine the interior

condition of electrical cabinets and control panels for cracks in frames, termination

and component integrity; instrument or wire damage

  • Reviewed the plant computer systems (PCS) raw data sequence of events to

determine whether equipment performed as expected or abnormal indications or

alarms were received during or subsequent to the seismic event

  • Reviewed electrical distribution system voltage and current chart recordings during

and subsequent to the seismic event

The team evaluated the performance of the supervisory and protection relaying and

lockouts for the sites electrical distribution system:

  • Reviewed CRs generated during and subsequent to the seismic event pertaining to

electrical system protection, relays, flags and spurious breaker actuations

  • Interviewed licensee staff to discuss all relay flags, lockouts and trips to determine

how each protective function was addressed

  • Reviewed vendor documentation on associated protection devices

The team reviewed the performance of the RSSTs, and others where applicable, in

response to the seismic event and the probable cause(s) of the transformers failure:

  • Reviewed design drawings associated with the station switchyard and substation.
  • Conducted interviews with licensees electrical power and transmission and

distribution personnel involved in the licensees review and investigation

  • Reviewed the sequence of events and alarm data to develop a comprehensive

understanding of the event progression as well as the restoration of the RSSTs

The team evaluated the licensees implementation of vendor recommendations

regarding the performance of transformers during the seismic event.

Enclosure

28

b. Observations and Findings

The team identified one URI associated with 1J EDG frequency oscillations that is

described in this section. The team concluded that ground motion from the earthquake

was the probable cause of sudden pressure trips and bushing damage affecting some

transformers that contributed to the loss of offsite power.

4160VAC, 480VAC Electrical Buses - Normal and Emergency

The licensee did not identify any abnormal or erratic electrical issues during or

subsequent to the initial seismic event. The following relays were noted to have had

ground targets, which caused their associated breakers to trip:

U1 Station Service 4160V Bus 1A U1 Station Service 4160V Bus 1B

- Breaker 15A3 - Breaker 15B3

- Breaker 15A5 - Breaker 15B5

- Breaker 15A6 - Breaker 15B7

- Breaker 15A7 - Breaker 15B10

- Breaker 15A9

- Breaker 15A10

U2 Station Service 4160V Bus 2C U2 Station Service 4160V Bus 2A

- Breaker 25C6 - Breaker 2A

The licensee attributed the breaker trips to seismic induced vibration. These station

service breakers were not seismically qualified and not safety-related. Each occurrence

was evaluated to ensure no actual damage or fault existed and was subsequently reset.

The licensee took a tiered approach to evaluating the functionality and operability of the

electrical system. The first phase of this approach, post-shutdown, included focused

visual inspections of a preselected sample of safety and non-safety related electrical

equipment considered most likely to be damaged from a seismic event. These

inspections included 100 percent walkdowns of all equipment, external to operating

cabinets and electrical switchgear. No seismic related deficiencies were identified. The

approach was then expanded and subsequent internal visual inspections were

conducted in accordance with 0-GEP-30 Post Seismic Event Engineering Walkdown

and are categorized in the table below.

Component  % Complete Findings

Transfer Buses 100% No Seismic Damage Noted

4160V Switchgear 96% No Seismic Damage Noted

480V Load Centers 95% No Seismic Damage Noted

Batteries 100% No Seismic Damage Noted

  • Information obtained from OD 000442, Revision 0

Enclosure

29

100 percent of the internal inspections were not completed for the 4160V Switchgear

and 480V load centers due to the current plant configurations, which did not allow an

open cubicle inspection. A sample set of about 96% (53 of 55 breaker cubicles) of

4160V Switchgear was completed. Likewise, a sample set of about 95% (600 of 632

breaker cubicles) of 480V load centers was completed. The remaining 5% were not

internally inspected due to current plant configurations. The team confirmed that the

electrical cubicles that would not be inspected due to plant configurations were

inspected on a periodic frequency consistent with the licensees preventive maintenance

program.

At the time of the Augmented Inspection observations, the licensee had completed

visual-only inspections of the electrical system equipment. The licensees Mode 5

Operability Determination (OD) 000442 stated that no deficiencies were identified that

would prohibit any system component from being considered functional and fully capable

of performing its design function. The team questioned relying on the results of visual

walkdowns and inspections to determine electrical equipment reliability. The licensee

indicated that further inspection and full surveillance testing would be conducted on

electrical system equipment prior to its return to a fully operable status. The licensee

had developed a recovery plan for the electrical system, which included the following:

  • Calibration and functional testing of protective relaying for all electrical equipment

4160VAC, main generators, oil-filled transformers, and transfer buses

  • 18 month PMs and PTs for all safety related electrical equipment
  • Dead bus inspections of 4160V bus work and fast transfer post maintenance tests

(PMTs) and verification

  • Crawl-through visual inspections of the interior of both units isophase bus duct,

which included all insulators and bus work

  • Segregated isophase bus duct hi-pot/megger testing for both the main and station

service transformers to identify any potential leakage current which would be

indicative of damaged insulator material

  • De-energized disconnect switch inspections

Based on interviews with the licensees electrical power personnel involved in the

investigation, independent review of licensee inspection activities and independent

random equipment selection for visual inspection, the NRC inspection team concluded

that the licensees actions with regard to these electrical perturbations were appropriate.

EDG

Following the seismic event and the subsequent LOOP, all four station EDGs started

and loaded onto their respective emergency buses. The AAC DG started automatically

and was manually aligned to the proper bus. All relay logic and load sequencers

appeared to have worked properly during the initial event. No unexpected alarms

related to the station EDGs were received at the onset of the event. About 45 minutes

after the seismic event, the 2H EDG developed a coolant leak that required the engine to

be manually secured. A diesel trouble alarm was received in the control room during

Enclosure

30

this time period due to alarms at the local control panel. Although a confirmed record of

which alarms were locked in was not available, firsthand accounts from the event did not

reveal any unexpected conditions. Annunciators associated with the jacket water

coolant leak were lit on the local annunciator panel following engine shutdown, all of

which were expected based on current plant conditions. The licensee did not identify

any instrumentation, relay or breaker issues that negatively impacted the EDG

performance during the response to the seismic event. Report Section 5.0 provides a

more detailed account of EDG performance and the 2H EDG jacket water coolant leak.

1J EDG Frequency Oscillations

Following the seismic event on August 23, 2011, while the 1J EDG was supplying power

to the 1J emergency bus, control room operators identified frequency oscillations on the

1J EDG bus as well as 1-III and 1-IV inverter momentary trouble alarms when the

pressurizer heaters were cycled. During personnel interviews, bus frequency was

reported as oscillating between 59 and 61Hz. The inspectors noted a Technical

Specification Limit of 59.5 and 60.5Hz. Engine load cycled between 1600 and 2000KW

while the 1J EDG was supplying power to the bus, varying as pressurizer heater loads

cycled. The PCS did not have a data point for emergency bus frequency so actual

emergency bus frequency was not recorded and could not be conclusively obtained.

The licensee entered this issue into the corrective action program as CR 440231.

There was a PCS data point that indicated engine speed (rpm), which could have been

used to calculate frequency with quality data available; however this PCS point for the 1J

EDG was very noisy during the event and could not provide any useful data to determine

the magnitude of frequency oscillations. All four EDG speed points on the PCS were

trended using engine run data since the seismic event occurred. Each engine was

operating parallel to the grid (stable at 900rpm) to observe stability of the data point.

There was noise in each data point: 1H, 2H and 2J showed oscillations of 20-30rpm

when paralleled and had a nominal speed indication between 895 and 920rpm. The 1J

data point showed oscillations of 100rpm in isochronous mode and when paralleled to

the grid and could therefore not be used to conclusively determine the 1J emergency

bus frequency. This data point was used for indication only and was not related to

actual engine stability.

On September 5, the licensee conducted a PMT of the 1J EDG in manual mode. During

that run, a troubleshooting sheet was prepared in response to CR 440231 and qualified

test equipment was used to measure engine frequency/voltage, electronic governor null

voltage, and the PCS rpm data point. Frequency responded as expected when control

was switched from the mechanical governor to the electric governor actuator and was

measured stable at 60.2Hz. The licensee was not able to test the 1J EDG in

isochronous mode, which was the configuration during the event due to current plant

conditions; however, the licensee was scheduled to recreate the scenario during the

upcoming refueling outage. The engine RPM indication is a separate issue that may

also be addressed during this evolution. An unresolved item will be opened pending

completion and results of licensee testing. This issue will be identified as URI

05000338, 339/2011011-04, 1J EDG Frequency Oscillations.

Enclosure

31

Distribution System

The North Anna Power Station switchyard consists of three single phase, generator

step-up transformers (GSUs), one per unit, which supply normal power to the station

through two, 3-phase SSTs. There are three, 3-phase RSSTs, shared between both

units, which are the preferred source of supply power to the emergency buses. Within

seconds of the seismic event, GSUs 1-EP-MT-1A; 2-EP-MT-1A, 1B, 1C; all RSSTs; SST

1-EP-SST-1C and switchyard transformer #2 all tripped due to sudden pressure relay

actuations, thereby causing a LOOP to both units. The licensees systems engineering

and control operations personnel conducted visual inspections of the distribution system

equipment and relay flags/targets were recorded and addressed. The likely cause of

relay actuations was attributed to seismic induced vibrations experienced during the

seismic event.

The 230kV line tripped and locked out due to a line-to-line fault from an offsite

substation. This perturbation was automatically isolated and did not have any adverse

affect on the North Anna switchyard or any plant parameters, however it was recorded

by the switchyard digital fault recorder. No other protective relay targets or deficiencies

were identified. The licensees corporate Fault Analysis Group reviewed the fault

recorder data in the switchyard remotely and determined that no fault current was seen

flowing through the transformers onsite during the seismic event. This figure will aid in

understanding the details of this event.

Enclosure

32

Figure 12, North Anna Simplified Electrical Power Distribution

The sudden pressure relay is designed to minimize the possibility of transformer tank

damage resulting from internal pressure buildup by detecting rates of pressure increase

in excess of the safe limits established by the transformer manufacturer. According to

vendor documentation, the relays are designed such that they will not be actuated by

vibration, mechanical shock, or pump surges. However it was noted in the vendor

information that vibration amplitude of installed relays should be minimized. Changes in

transformer internal pressure deflect a sensing bellows and responding control bellows

that are part of a closed hydraulic system filled with silicone oil. A temperature

compensating control orifice in the line of one of the control bellows causes differential

deflection of the two control bellows when fluid flow in the system exceeds calibrated

values. As this differential deflection occurs, a linkage positioned on these control

bellows actuates a snap switch, tripping a circuit breaker that de-energizes the

transformer. When equilibrium between the two control bellows is reached, the snap

switch resets automatically.

Each phase of the station GSUs has three sudden pressure relays installed horizontally

on the tank wall along the same plane. The GSU circuit breakers open and lockout

when two out of the three sudden pressure relays are actuated on either phase. This de-

energizes the SSTs and the normal power supply to the station. The RSST circuit

breakers open and lockout when a singular sudden pressure relay is actuated, thereby

Enclosure

33

de-energizing the preferred power supply to the emergency buses. During the seismic

event, the following sudden pressure relays actuated:

Unit 1 GSUs - TRIPPED Unit 2 GSUs - TRIPPED

Phase A: 3 Relays (3 Actuated) Phase A: 3 Relays (3 Actuated)

Phase B: 3 Relays (0 Actuated) Phase B: 3 Relays (3 Actuated)

Phase C: 3 Relays (0 Actuated) Phase C: 3 Relays (3 Actuated)

Unit 1 SSTs - TRIPPED Unit 2 SSTs - NO TRIP

Phase A: 3 Relays (0 Actuated) Phase A: 3 Relays (0 Actuated)

Phase B: 3 Relays (1 Actuated) Phase B: 3 Relays (0 Actuated)

Phase C: 3 Relays (3 Actuated) Phase C: 3 Relays (0 Actuated)

RSSTs - ALL TRIPPED 36.5kV XFMRs - TX 2 TRIPPED

RSST A: 1 Relay (1 Actuated) TX 1: 3 Relays (0 Actuated)

RSST B: 1 Relay (1 Actuated) TX 2: 3 Relays (3 Actuated)

RSST C: 1 Relay (1 Actuated) TX 3: 1 Relays (0 Actuated)

The licensees electric transmission and distribution personnel evaluated the probable

causes of the sudden pressure relay operation. The following were preliminarily

identified:

  • Sudden pressure rise in the transformer oil tank was caused by the earthquake

vibrations. Basis: When a transformer is subjected to the three-dimensional random

ground motions of the magnitude experienced at the station, substantial forces

produce vertical and horizontal accelerations, which will cause a rapid pressure rise

on the sudden pressure relay, thereby inducing actuation.

  • Improper operation of the sudden pressure relay mechanism. Basis: The impact of

the seismic vibrations on the springs and micro-switch internal to the relay may

cause the micro-switch to operate improperly. The seal-in package will permanently

preserve the improper operation of the relay before a manual reset occurs. Two

relays could operate improperly at different times and the 2 out of 3 voting scheme

will still trip the lock-out due to the memory of the relays internal seal-in package.

  • Relay seal-in circuit malfunction. Basis: It is possible, however unlikely, that the

normally opened and normally closed contacts of the auxiliary relays that create the

seal-in circuit (diagramed below) could both change state inadvertently at the same

time, due to the seismic event and thereby energize the auxiliary relay. The two

contacts would be actuated and the relay would remain in the improper state.

Enclosure

34

Figure 13, Dominion Seal-In Package Schematic

The licensee noted that thorough seismic tests and analysis need to be performed on

the sudden pressure relay and the Dominion in-house seal-in circuit to confirm or refute

their possibilities as the root cause of the sudden pressure relay operations.

The team also reviewed the electrical distribution system voltage and current chart

recordings during and subsequent to the seismic event. There were no indications of

electrical faults present on the switchyard side of the GSUs on Unit 1 or Unit 2. There

were no indications from the chart recordings or the Digital Fault Recorders (DFRs) of

electrical faults on the 34.5kV buses. The chart recordings indicated that Unit 1 GSUs

tripped first and voltages were still present for about four cycles likely as a result of the

lowside unit breaker at the site opening slightly later than the breakers in the switchyard.

The Unit 2 GSU voltages remained and eventually decayed over time due to the residual

field voltage.

After review of vendor information, interviews with the licensees electrical personnel

responsible for this investigation and review of the licensees cause evaluation for the

actuation of the sudden pressure relays, the team concluded that the protective relaying

functioned as expected when subjected to a seismic event. This equipment is not

seismically qualified and can be susceptible to actuation resulting from pressure rises

caused by seismic activity. The team also concluded that all recorded data showed that

the electrical distribution system equipment functioned as expected with no signs of

electrical faults. The licensee was evaluating several mitigation options with regard to

supervisory and protection relaying in effort to make the emergency offsite power source

more reliable during future seismic events.

Enclosure

35

Switchyard Damage

The licensee initiated walkdowns and conducted visual inspections of the switchyard and

the RSSTs to verify the status of offsite power. Technicians noted oil leaks from all six

of the GSUs. As a result of the seismic event several high voltage bushing seals were

compromised. A total of eight 500kV bushings were damaged on Unit 1 and 2 GSUs

(six main transformers and two spares). The licensees transmission and distribution

personnel identified that, in all cases, the upper porcelain shifted and compromised the

lower seal between the busing flange and upper porcelain. The bushings were not

seismically qualified and are therefore susceptible to damage and failure during a

seismic event. This issue was entered into the licensees corrective action program.

The bushings were scheduled to be returned to the vendor for inspection, test,

disassembly, and re-gasket. The licensee was also evaluating the procurement of

seismic rated bushings to replace the damaged bushings as a long-term mitigation

option.

On September 10, 2011, while performing routine maintenance on the current

transformer for the 500kV generator breaker G202 on Unit 2, the licensee removed the

upper bellows protective cover for inspection and identified that some of the support

blocks had broken and the lower bellows support arm had been displaced. The

transformers were not seismically qualified and are therefore susceptible to damage and

failure during a seismic event. All six current transformers on Unit 2 were subsequently

inspected and no additional damage was identified. The licensee attributed this damage

to have been caused by the seismic activity due to the earthquake. The licensees

electric transmission and distribution personnel were reviewing this issue and current

transformers for Unit 1 generator breakers were scheduled to be inspected prior to

switchyard restoration.

Restoration of RSSTs

The licensees systems engineering and control operations personnel performed the

following actions to verify the status of the RSSTs after the seismic event:

  • Main tank, bushings, and load tap changers (LTC) were inspected for damage and

oil leaks

  • Nitrogen supply, overhead 4kV bus connections (secondary side), transformer pads,

tube bus and cables, lightning arrestors and control cabinet equipment were all

visually inspected for damage

  • The 480VAC supply from the station to the control cabinet was verified by checking

the LTC controllers in the A and C RSSTs and all annunciator flags/targets were

recorded and addressed

  • The position indicator on the LTC was verified to be in the appropriate position and

all ground connections to the main tank were intact

Licensee personnel reported that all electrical connections and physical conditions for

the RSSTs appeared to have performed satisfactorily during the event.

Enclosure

36

All three RSSTs tripped and locked out due to their respective sudden pressure relay

actuations on one-out-of-one logic devices. The licensee also confirmed the status of

the differential relays in the Emergency Switchgear Room monitoring the RSSTs and

noted that there were lockouts for each RSST, but no relay targets. No other abnormal

indications were identified. The licensees corporate Fault Analysis Group reviewed the

fault recorder data in the switchyard remotely and determined that no fault current was

seen flowing through the transformers onsite during the seismic event. The licensee

then locally performed a dissolved gas analysis (DGA) on the RSSTs in the priority of

RSST C, B, then A. This was a decision made by the technical support staff in the

Technical Support Center (TSC). Priority was given to RSST C because its supply bus,

34.5kV bus #3 was available, which normally supplies power to the 1H and 2J

emergency buses. In addition, RSST C supplies power to the TSC through the Unit 2 G

bus, which has a crosstie capability allowing it to supply power to the Unit 1 G bus using

the 15G10 breaker. It should be noted that the 15G10 breaker had an 86 lockout

present due to a station load shed signal being present. The station load shed actuated

from the SSTs and GSUs tripping earlier in the event. This lockout delayed the return to

service of the 15G10 breaker. RSST C was released and restored at about 4:30 p.m. on

August 23. RSST B was given second priority and would supply power to the 2H

emergency bus and the 1G bus, which is its normal supply. This would also allow the

SBO diesel to be secured, which was supplying power to the 2H emergency bus as a

result of the jacket water leak on the 2H EDG. Before RSST B was restored to service,

the licensee aligned it to the 34.5kV bus #5 due to the switchyard Transformer #2

lockout from its sudden pressure relay, which had not yet been fully restored. RSST B

was released and restored at about 5:30 p.m. on August 23. Lastly, at about 6:30 p.m.

RSST A was restored which would supply power to the 1J emergency bus. Transformer

  1. 2 was subsequently evaluated and released at about 7:00 p.m. on August 23, 2011.

Vendor Recommendations Regarding Transformer Response During Earthquakes

RSST A and C are original to the station. RSST B was replaced in March of 1985. Both

Unit 1 and 2 have newer GSU transformers, which were installed in 2004 and 2005,

respectively. Neither GEK-35003, General Electric Instruction Manual for Reserve

Station Transformers nor VTM-59-M947-0003 GSU Transformer Replacement for

Units 1&2 specify recommendations to prevent or mitigate the effects of a seismic event

on the installed transformers. Likewise, these documents did not stipulate a service or

end of life for the transformers. The licensee indicated that the preventative

maintenance program monitors dissolved gases and trends equipment performance to

determine the need to replace equipment. The team reviewed the transformers

component health report, which reflected deficiencies independent of the seismic event.

The team did not identify any issues in this report affecting seismic vulnerability. There

were no indications of issues with regards to dissolved gases, however the licensee

planned to replace the RSSTs and upgrade the electrical power system in the near

future.

Enclosure

37

7.0 On-Shift Human Performance

The team conducted an overall and independent review of On-shift Human Performance

to determine if licensee staff responded properly during the event, procedures were

adequate, and to better understand the licensees decision making process. The

following areas were specifically addressed and are discussed in more detail in the

following sections:

  • Determine whether emergency operations procedures (EOPs) were performed

consistent with training

  • Verify that the SBO DG was placed into service consistent with the procedures
  • Verify proper and timely response to identifying and reacting to the 2H EDG failure
  • Review the restoration of offsite power through the RSSTs
  • Review the timeliness and adequacy of Emergency Planning declarations during the

event

  • Evaluate immediate operator response with regard to the guidance in Regulatory

guide 1.166, Pre-Earthquake Planning and Immediate Nuclear plant Operator Post

Earthquake Actions

Additionally, the team reviewed the licensees corrective actions, causal analysis, and

extent of condition, with respect to On-shift Human Performance.

7.1 Emergency Operating Procedures (EOPs)

a. Inspection Scope

The team conducted an independent review of control room activities with respect to the

EOPs to determine if licensee staff responded properly during the events. The team

also reviewed the licensees implementation of abnormal, alarm and normal operating

procedures used during the event. The review included the effectiveness of the

procedures in addressing the event. With respect to operator awareness and decision

making, the team was specifically focused on the effectiveness of control board

monitoring, communications, technical decision making, and work practices of the

operating crew. With respect to command and control, the team specifically focused on

actions taken by the control room leadership in managing the operating crews response

to the event. The team performed the following activities in order to understand and/or

confirm the control room operating crews actions to diagnose the event and implement

corrective actions:

  • Conducted interviews with control room operations personnel on shift during the

event

  • Reviewed procedures, narrative logs, event recorder data, system drawings, and

plant computer data

  • Reviewed the crews implementation of emergency, abnormal, and alarm procedures

as well as Technical Specifications

Enclosure

38

  • Reviewed Operations administrative procedures concerning shift manning and

procedure use and coordination

b. Observations and Findings

The team concluded that EOPs were performed consistent with training. The team

determined that operators exhibited fundamental operator competencies when

responding to the event while using EOPs. Specifically, the team determined that the

operating crew identified important off-normal parameters and alarms in a timely manner

for the external seismic event and the subsequent LOOP. Additionally, the team

determined that crew supervision exercised effective oversight of plant status, crew

performance, and site resources.

Monitoring of Plant Parameters and Alarms

Through a review of plant data, the team determined that the crews response to the

seismic event was effective in stabilizing the plant. Through interviews and review of

plant data, the team determined that the crew recognized the seismic event and

resulting LOOP. Based on interviews, the on-shift crews for each unit assessed the

plant conditions as being consistent with what was experienced during simulator training

for a LOOP.

Based on the sequence of events, a review of plant data, and operator interviews, the

team concluded that the LOOP prevented the normal access to plant online Alarm

Response Procedures (ARPs) because the document server was powered from offsite

power. The procedures were available in the control room as paper copies. EOPs and

Abnormal Procedures (APs) were readily available during the event with no delay.

Based on operator interviews, the team concluded that the operators completed a

satisfactory review and evaluation of alarm conditions after the event.

Command and Control

Based on NRC inspector observations during the event and interviews and a review of

plant data, the team determined that the Shift Manager (SM) and Shift Technical Advisor

(STA) maintained oversight of the plant, which included awareness of major plant

parameters such as RCS temperature and pressurizer level, during the event. Based on

observation and interviews, the team determined that the SM effectively managed the

frequency and duration of crew updates and crew briefs during the event. Crew updates

were reasonable based on the implementation of EOPs. The team concluded that the

SM and Control Room Supervisor (CRS) ensured monitoring and diagnosis of key major

plant parameters, such as RCS temperature, pressurizer level, and VCT level, by control

room crew members.

Based on a review of plant data, the team concluded that the management expectation

for establishing positive control of equipment configuration was implemented by the

operating crew. Through interviews and a review of plant data and alarm response

Enclosure

39

procedures, the team determined that the SM and CRS ensured that sufficient

information necessary to assess abnormal electric plant status was collected and

evaluated prior to performing steps within a procedure that assumed a normal electric

plant configuration.

During interviews, operators stated that the loss of the document computer for ARPs

was not a common scenario in training packages. The licensee was considering

addressing this in their training program. The team determined that the loss of the

document computer only affected ARPs and did not significantly affect operator

performance during the event.

Resource Utilization

Through interviews, the team determined that the Balance of Plant (BOP) operators and

off-shift operators were available to assist the control room operators in recognizing and

diagnosing off-normal issues. The seismic event occurred on dayshift which provided

additional resources to the control room crew. The utilization of operators during the

dual unit trip was adequate.

Other Operating Procedures

The team observed that procedure 1-AR-F-D8, Turbine Driven AFW Pump Trouble or

Lube Oil Trouble did not state that the low lube oil level switch was powered from non-

vital power. Upon a loss of power, the lube oil level switch will generate an alarm signal

and the alarm, which has a different power source, will activate. The alarm procedure

did not recognize this issue. During interviews, operators revealed they were unsure as

to why the alarm was lit and the issue required additional troubleshooting. This resulted

in a short delay in the alignment of the Unit 1 terry turbine AFW pump to the steam

generator. An unresolved item will be opened pending completion of this review. The

issue will be identified as URI 05000338, 339/2011011-05: Unit 1 Turbine Driven

Auxiliary Feedwater Pump Trouble Alarm.

7.2 Station Black-Out Diesel Generator

a. Inspection Scope

Information was obtained from inspector observations during the event, interviews with

the operating crew, system descriptions, event sequence of event, plant computer data

and narrative logs to support this review. The team reviewed operator performance to

determine whether operator actions were consistent with approved procedures, TS, and

training. The team compared this to training received for a LOOP and the plant

response to this event as demonstrated by the operation of the SBO DG.

b. Observations and Findings

The team concluded that operators responded in accordance with procedures for the

SBO DG and that training contributed to the understanding of the plant response during

Enclosure

40

the event. The team did not identify significant issues related to operator response

during the LOOP event for the operation for the SBO DG.

The team observed that procedure OP-6.4 Operation of the SBO Diesel (SBO Event)

contained a step to insert a synch key required for alignment of the SBO DG. The key

was not readily available to the crew in the field during the event. This resulted in delay

of about 7 minutes in the alignment of the SBO DG to the 2H bus. The team determined

that the delay was not consequential during this event. The licensee included this issue

in their corrective action program.

7.3 2H Emergency Diesel Generator Failure

a. Inspection Scope

Information was obtained from inspector observations during the event, interviews with

the operating crew, system descriptions, event sequence records, PCS data and

narrative logs to support this review. The team reviewed operator performance to

determine whether operator actions were consistent with approved procedures,

Technical Specifications, and training. The team compared operator response to

training received for a LOOP and the plant response to this event as demonstrated by

the operation and subsequent failure of the 2H EDG.

b. Observations and Findings

The team concluded that operators responded to the 2H EDG failure in accordance with

approved procedures.

From interviews, the team determined that the control room operators, in responding to

the event, relied on actions and guidance described in APs. From a review of the plant

procedures used by operators to respond to this event, there were no significant issues

identified.

During operator interviews, when the LOOP was experienced, operators stated that

access to the EDG rooms was delayed because power was lost to some access control

systems. This affected normal access for personnel entering the plant after the event.

The team determined that procedures were implemented to make keys available to

security personnel and operators, and that delays experienced obtaining keys were not

consequential. The licensee included this issue in their corrective action program.

Enclosure

41

7.4 Restoration of Offsite Power

a. Inspection Scope

Information was obtained from inspector observations during the event, interviews with

the operating crew, system descriptions, event sequence records, plant computer data

and narrative logs to support this review. The team reviewed operator performance to

determine whether operator actions were consistent with approved procedures, TS, and

training. The team compared this to training received for a LOOP and the plant

response to this event as demonstrated by the operation and subsequent realignment of

the RSSTs.

b. Observations and Findings

The team concluded that operators responded in accordance with approved procedures

in the restoration of offsite power.

Based on interviews, the team determined that the SM used technical resources

available in the TSC for performing an assessment of damage to the electric plant before

the crew reset the RSSTs. The team noted that such assessments were able to

determine the sudden pressure lockout condition on the RSSTs. Report Section 6.0

provides additional discussion on restoration of offsite power.

The team determined that the licensee adequately identified and documented causes

specific to the event as well as immediate and proposed corrective actions.

7.5 Emergency Planning Declarations

a. Inspection Scope

The team reviewed the licensees implementation of the emergency preparedness (EP)

procedures used during the event. The review focused on the circumstances

surrounding the events to determine if the licensees EP classification and notifications

were appropriate and timely. The team interviewed members of the licensees

organization and other individuals involved with EP aspects of the event. The team

reviewed the event timeline, logs, statements by individuals who responded to the event,

the North Anna emergency action level (EAL) matrix, event notification worksheets, and

other documents related to EP classifications.

b. Observations and Findings

The team concluded that emergency planning declarations were appropriate. The team

identified one URI described in this section.

In order to determine the appropriateness of the EP classifications, the team performed

a detailed assessment of the event timeline with particular attention to those activities

that are entry points for the EAL matrix. On August 23, 2011, at 1:51 p.m., the site

Enclosure

42

experienced a magnitude 5.8 earthquake with an epicenter twelve miles southwest of

the plant. Both reactors tripped. A LOOP occurred at 1:51:12 p.m. All four EDGs auto

started to their respective emergency bus (1H, 1J, 2H, and 2J) at 1:51:20 p.m. An Alert

was declared at 2:03 p.m. for HA6.1, SM judgment, due to an inability to enter the

seismic EAL for seismic event because the seismic monitoring panel earthquake trouble

alarm to notify operators of a seismic event did not illuminate. HA1.1, earthquake

response, required that the strong motion accelerograph peak shock annunciator

illuminates, which would indicate a seismic event greater than OBE (0.06g horizontal or

0.04g vertical) and an earthquake confirmed by any of the following:

  • Control Room indication of degraded performance of any safety-related structure,

system, or component

The strong motion accelerograph peak shock annunciator did not illuminate.

The seismic monitoring panel has two recording systems, one provided by Kinemetrics

Inc. and the other provided by Engdahl. Both systems provide input to the main control

room via a common instrumentation panel on the Unit 2 side of the control room. All

sensors for the Kinemetrics system are located inside Unit 1 containment. The

Kinemetrics system has a seismic trigger, which activates at 0.01g in a any direction. In

addition, there is a seismic switch which activates at 0.04g vertical and 0.06 horizontal.

Neither the seismic switch nor the seismic trigger activated the earthquake trouble

alarm. Locally at the seismic panel, the seismic trigger was activated and a tape

recording of the event was recorded. Therefore, operators determined that the seismic

monitoring panel was inoperable for making a decision about the strength of the

earthquake. The team determined that the lack of control panel alarm from the seismic

monitoring panel did not delay an Alert declaration, because the SM used HA6.1, SM

judgment.

Because of the issues identified with the seismic monitoring panel and because it is

used as an input for EAL decisions, additional review by the NRC will be needed to

determine whether this issue represents a performance deficiency. An unresolved item

will be opened pending completion of this review. The issue will be identified as URI

05000338, 339/2011011-06: Seismic Alarm Panel.

Personnel in the plant monitoring the 2H EDG reported the coolant leak to the control

room via face-to-face communication. Operators tripped the 2H EDG at 2:40 p.m. An

Alert was declared at 2:55 p.m. for SA1.1, AC power, for Unit 2, because the AC

capability was reduced to a single source with 2J EDG.

The team determined that notifications to the State and Counties and to the NRC

Operations Center were timely and accurate.

The Alert event was downgraded to a Notice of Unusual Event (NOUE) at 11:16 a.m. on

August 24, for HU1.1, seismic activity, due to the potential for aftershocks. The NOUE

Enclosure

43

was exited on August 24, 2011, at 1:15 p.m. The decision to terminate the event was

based on the following: (1) no public issues existed that would necessitate the

continued activation of the State and County Emergency Operations Facilities; (2) the

licensees Outage Control Center had established a technical focus and was aligned for

the recovery activities; and (3) no additional aftershocks were received at the plant. The

team determined that downgrade of the Alert event at 11:16 a.m. was appropriate.

7.6 Post Earthquake Actions

a. Inspection Scope

The team reviewed the licensees processes and procedures established to adequately

plan and respond to a post seismic event in accordance with Regulatory Guide (RG)

1.166, Pre-Earthquake planning and Immediate Nuclear Power Plant Operator Post-

Earthquake Actions, dated March 1997. The team reviewed multiple procedures used

to respond to a seismic event. The team also conducted interviews with the licensee

personnel involved in the response to the seismic event. The seismic data collected after

the event and manner in which this data was collected and processed was evaluated by

the team. Finally, the team reviewed relevant/critical CRs developed during the

licensees post seismic assessment.

b. Observations and Findings

Although the licensee is not committed to RG 1.166, based on the review conducted by

the team, the licensees program deviates from the guidance in this RG as listed below:

  • Part B of the RG specifically states, This regulatory guide is based on the

assumption that the nuclear power plant has operable seismic instrumentation,

including the computer equipment and software required to process the data within 4

hours after an earthquake. The staff at North Anna at the time of the inspection did

not have a documented procedure or the ability to process the seismic data within

this time frame. Operators were unable to determine within four hours whether the

operational basis earthquake was exceeded in accordance with Section C.4 of RG

1.166.

  • Regulatory Position 3.2.1, states, Only personnel trained in the operation of the

instrument should collect data. This statement is specifically in reference to seismic

instrumentation used to collect seismic data. Through interviews with the licensee

staff it was determined that at the time of the inspection a procedure to collect data

did exist but there were no members of the staff trained to implement the procedure.

  • Part B of the RG specifically states, The data from the nuclear power plant's free-

field seismic instrumentation, coupled with information obtained from a plant

walkdown, are used to make the initial determination of whether the plant must be

shut down, if it has not already been shut down by operational perturbations resulting

from the seismic event. At the time of the inspection no free-field seismic

instrumentation existed as assumed by RG 1.166.

Enclosure

44

As previously mentioned the licensee is not committed to RG 1.166.

The team determined that the seismic monitoring panel earthquake trouble alarm,

intended to notify operators of a seismic event, did not illuminate. The operators did not

see the control panel alarm lit after the earthquake, after the LOOP, or after the

emergency buses were powered from the EDGs. Operators determined that the seismic

monitoring panel was inoperable for making a decision about the severity of the

earthquake. Operators were therefore unable to make a rapid determination of the

degree of severity of the seismic event. The portion of the seismic monitoring panel that

provides immediate feedback as to the severity of the earthquake lost power during the

LOOP. It was powered from non-vital power. In addition, the panel has no electronic

memory. The magnetic tape recording system, which had a back-up power supply,

recorded the event. Additional discussion of this issue is in Section 7.5.

The team made the following additional observations with regard to RG 1.166:

  • The seismic event tripped both Unit 1 and 2 reactors and the decision to shutdown

was not required based on seismic monitoring equipment.

  • Operators and engineers were able to conduct plant walkdown inspections within

eight hours of the event and discovered no significant damage to plant systems in

accordance with EPRI NP-6695 as recommended with Section C.1.2 of RG1.166.

  • Operators were able to take actions immediately after the earthquake in accordance

with Section C.2 of RG 1.166.

  • Operators were able to take some actions for data collection after the earthquake in

accordance with Section C.3.2 of RG 1.166.

  • The licensees procedure, AP-36, Seismic Event, incorporated guidance in Appendix

A of RG 1.166, but operable seismic instrumentation and equipment (hardware and

software) to process the data was not available. The licensee would have been able

to determine if OBE was exceeded by following Appendix A because an earthquake

of magnitude 5.0 or greater had occurred within 200km of the plant.

Enclosure

45

8.0 Plant Parameters and Assessment

8.1 Unexplained Instrumentation Anomalies

a. Inspection Scope

During the post event review, the licensee identified some unexpected anomalies that

occurred during the event, related to safety related instrumentation. The team

independently reviewed event recorders, plant records, and interviewed personnel to

determine whether the licensee had identified and appropriately addressed any

observed equipment performance issues.

b. Observations and Findings

The team found that some plant instrumentation anomalies warranted follow-up. The

team identified one URI described in this section.

The licensee had identified and recorded a number of instrument anomalies, many of

which were attributed to the earthquake. Some examples of instruments affected

included:

  • Minor perturbations in Units 1 and 2 Safety Injection Accumulator and Refueling

Water Storage Tank (RWST) levels

  • Nuclear Instrumentation
  • Loop 1C High Delta Temperature
  • RWST Chemical Addition Tank Temperature

The team questioned whether these anomalies were indications of actual parameter

changes in level, pressure, etc. due to the seismic event or false indications that were

seismically induced. If the indications were seismically induced, the team inquired

whether the instrument exceeded their seismic qualification or whether the seismic

qualification of the instrument was appropriate. The licensee planned to determine the

most likely cause of the anomalies through their root cause assessment of the August

23, 2011 seismic event.

Because some of the anomalies identified with the safety related instrumentation could

have been seismically induced and thus potentially calls into question the seismic

qualification of the instruments, additional review by the NRC will be needed to

determine whether this issue represented a performance deficiency. An unresolved item

will be opened pending completion of this review. The issue will be identified as URI

05000338, 339/2011011-07: Safety Related Instrumentation Anomalies.

Enclosure

46

8.2 General Assessment

a. Inspection Scope

The team reviewed the licensees Probabilistic Risk Assessments (PRA) to select the

most risk significant systems and associated structures for physical walkdowns and

review. Sections 5.0 and 6.0 of this report contain additional information on walkdowns

and reviews of electrical systems. In addition, the team reviewed the licensees

Independent Plant Examination for External Events (IPEEE) report to identify structures

and systems most vulnerable to seismic activity for walkdowns and review. In addition

to selecting samples based on PRA and IPEEE, the team conducted general plant

walkdowns to include areas of potential interest, including but not limited to the Spent

Fuel Pool and the North Anna Dam.

The team observed walk-downs of safety related systems conducted by the licensee.

The team reviewed design drawings associated with the specific systems inspected by

the licensee. In addition, the team conducted walkdowns of systems already completed

by the licensee to verify any post seismic event damage was adequately documented by

the licensee. Historical walkdowns of systems and components conducted due to

routine maintenance were reviewed to determine if documented issues were classified

properly (new or existing). The team also conducted interviews with the licensee

personnel involved in the response to the seismic event. The seismic design

methodology contained in Final Safety Analysis Report (FSAR) was also reviewed to

determine the DBE for all safety-related structures and components. Finally, the team

reviewed relevant/critical CRs developed during the licensees post seismic assessment.

b. Observations and Findings

Based on the scope of the inspection, the team found no significant damage to the plant

related to the earthquake. Some equipment issues were experienced, as documented in

this report.

The licensee had assembled a seismic event response team to assess the overall

condition of safety-related system, structures, and components (SSC). The licensee

drafted two post seismic event inspection procedures based on EPRI Technical Report,

NP-6695, Guidelines for Nuclear Plant Response to an Earthquake, dated December

1989. The two procedures were established to provide guidance for structures and

systems visual inspections. The team reviewed procedure ER-NA-INS-104, Monitoring

of Structures North Anna Power Station, Revision 1 for structures that meet the

regulatory Requirements for Maintenance Rule and License Renewal that contribute to

the operation of the station. Procedure 0-GEP-30, Post Seismic Event System

Engineering Walkdown, Revision 1 was also reviewed for adequacy. This was used by

licensee personnel to provide guidance for performing a general condition assessment

of system based SSCs following a seismic event. During the review of these procedures

the inspection team noted a common issue in both procedures, in that neither procedure

directed its user to review past inspection history to determine if observed damage is

pre-existing or post seismic event damage. Conservatively all damage found was

Enclosure

47

documented in a Deficiency Log and a corresponding CR was drafted. All damage

found was then cross-referenced on with previous historical inspection to determine if

the condition was a post-event issue or previously identified. This action was not

proceduralized but was currently being implemented by licensee staff conducting walk-

downs related to post-inspected activities.

The team directly observed a sample of walk-downs conducted by the licensee

engineering staff. Prior to the inspection observation, the pre-job brief was observed by

the team to verify safety and technical guidance was provided to licensee staff

conducting inspections. This briefing also verified that staff conducting walk-downs were

properly trained and qualified to the procedure being implemented.

After walkdowns were completed by the licensee, their plan was to conduct

Nondestructive Examination (NDE) on a sampling basis prior to start-up. This was

referred to as Owner Elective examinations above and beyond the requirements of their

Inservice Inspection (ISI) program. The NDE will be performed on a sample of

components based on previous NDE conducted prior to the earthquake to provide a

baseline for the NDE results.

In North Annas IPEEE report, seismic margin assessment was used with a review level

earthquake of 0.3g and a spectral shape given in NUREG/CR-0098. Only 13

component types were found to have a High Confidence of Low Probability of Failure

(HCLPF) capacity less than 0.3g and these components are identified in Table 3.2-1 of

the licensees IPEEE report. The licensee performed walkdowns of these components

with qualified and trained seismic review teams. The team reviewed the results of the

completed walkdown inspections performed by the licensee for these components. The

licensee had not completed these inspections for 120V AC Bus and 4160V emergency

buses at the time of the teams review. Based on inspections conducted at the time of

the review, the licensee had not identified any damage that was earthquake related.

However, the licensee had found several non-structural issues, e.g., grout cracking,

improperly installed bolt, insulation banding coming loose, and loose nuts, which the

licensee concluded were not earthquake related. These conditions were previously

identified during baseline inspections prior to the earthquake. The licensee issued a

number of CRs to correct these conditions.

The inspectors selected a representative sample of systems for walkdown based on

HCLFP capacity. These systems included Emergency Condensate Storage Tanks,

Refueling Water Storage Tanks, Refueling Water Chemical Addition Tank (Unit 1), and

Control Room Air Conditioners. The team also reviewed some design calculations for

selected components for determination of HCLPF capacities.

The team conducted a number of general plant walkdowns. The following includes the

results of system walkdowns, including those selected based on IPEEE HCLFP reviews,

where the team conducted a focused sample or where observations were made.

Enclosure

48

Safety Injection System

The Safety Injection (SI) System as part of the Emergency Core Cooling System (ECCS)

will provide borated emergency cooling water to the reactor core for the entire spectrum

of RCS break sizes to limit core temperature, maintain core integrity, and provide

negative reactivity for additional shutdown capability. The Low Head SI System provides

core cooling in the event of a Design Basis Loss of Coolant Accident (LOCA), it provides

flow to the High Head SI pumps in the event of a safety Injection, and provides backup

core cooling during shutdown and refueling.

The team accompanied the licensee engineering staff on walkdowns of the SI system for

Unit 1. This inspection included an assessment of the SI low-head A and B injection

pumps for seal leaks and structural support damage. The inspections included pipe

sections leading into containment penetrations 61 and 62 for weld cracks and damage to

the penetrations entry points. The 1-SI-MOV-1885A and 1-SI-MOV-1885C MOVs were

also inspected for yoke crack and support damage due to the seismic event. Snubbers

were inspected for leakage and damage. These components were identified on drawing

11715-FM-096A to track the specific areas inspected. All walkdowns for the SI system

were completed during the time of inspection. The licensee was in the process of

conducting functional and performance testing to fully qualify this system. Based on

successful resolution of discrepancies noted during walkdowns, satisfactory testing of

SSCs and satisfactory performance, the SI system was considered operable/functional

but not fully qualified on Units 1 and 2 for Mode 5. Additional performance tests were

planned in order to make the system operable for all modes as a path to reactor start-up.

Service Water System

The Service Water (SW) system provides vital cooling to the following components

during normal and accident conditions: Core Cooling Heat Exchanger, main control room

chillers, charging pump lube oil coolers and gear box coolers, and the Instrument Air

coolers. Additionally, a 22.5 million gallon spray pond provides the function of Ultimate

Heat Sink when heat is transferred from the Recirculation Spray Heat Exchangers

(RSHX) to the SW system following a Containment Depressurization Actuation. The SW

system also provides backup cooling to the Spent Fuel Pool, Aux Feed Water system,

and Containment Air Recirculation Fan coolers in the event the normal cooling supply is

lost. The SW system is a diverse system consisting of four main SW pumps, two Aux

Service Water pumps, the spray pond, and two trains providing cooling to plant

components. During a Design Basis Accident, the SW system is cross-tied at the

RSHXs and acts as a single large system while still cooling both the accident and non-

accident units load.

The team conducted an independent walkdown of the SW pump and valve house for

Units 1 and 2. Prior to conducting the walkdown the team reviewed the walkdown

inspection report conducted by the licensee to identify areas of interest to the team. The

licensee SW system engineer accompanied the team during the walkdown to address

any questions the team had related to the system. This inspection was focused on an

assessment of the pump and valve house building structures and the condition of safety

Enclosure

49

related components located in these structures. Specifically, the SW A and B pumps for

Units 1 and 2 were inspected for seal leaks and structural support damage. The special

Technical Requirements for settlement of both structures were evaluated to determine if

any excessive differential settlement was observed due to the seismic event. Post event

survey readings were taken by the licensee but the results were not available at the time

of inspection. Water-hammer restraints were inspected for evidence of plastic

deformation of connections and anchorage. These components were identified on

drawings 11715-FM-096A to track the specific structural elements and components

inspected and to determine original design configuration of each SSC. All walk-downs

for the SW system were completed during the time of inspection. The licensee was in

the process conducting functional and performance testing to fully qualify this system.

Based on successful resolution of discrepancies noted during the walkdown, satisfactory

testing of SSCs and satisfactory performance, the SI system was considered

operable/functional but not fully qualified on Units 1 and 2 for Mode 5. Additional

performance tests were planned in order to make the system operable for all modes as a

path to reactor start-up.

Refueling Water Storage Tank

The RWST supplies borated water to the Chemical and Volume Control System (CVCS)

during abnormal operation conditions, to the refueling, and to the ECCS and the Quench

Spray System during accident conditions. This component is an IPEEE component and

has a seismic capacity less than 0.3g under their IPEEE. All other IPEEE systems and

components with seismic capacities less than 0.3g were given additional evaluations

under the Seismic Qualification Utility Group (SQUG), Generic Implementation

Procedure (GIP) for Seismic Verification of Nuclear Plant Equipment, Revision 2 (GIP-

2). The GIP-2 was developed by SQUG in response to Unresolved Safety Issue (USI)

A-46. This additional evaluation was to verify each component maintained the

requirements of the criteria established in the GIP-2.

During a review of the licensees design drawing (Drawing # 11715-FV-44A, Refueling

Water Storage Tank, Revision 7), the team identified a note that appeared to indicate

that the tank was designed for a horizontal acceleration of 0.69g and vertical

acceleration of 0.35g. Table 3.2-1 of the licensees IPEEE report indicates a HCPLF

value of 0.18g. The team requested a clarification of this discrepancy. The licensees

response indicated that the basis for the acceleration values shown on the drawing is not

known. The tank was evaluated during the licensees response to USI A-46 and IPEEE.

The team reviewed the licensees calculations in the A-46 evaluation (Calculation #

52308.04-C-004, A-46 Evaluation of Refueling Water Storage Tank, Revision 3, dated

March 15, 1999), and the HCLPF calculation, (Calculation # 52182-C-039, Seismic

Margin HCLPF Calculations for Refueling Water Storage Tank, Revision 2, dated April 5,

1997). The calculation documented the basis of the current HCLPF value of 0.18g for

the RWST. Based on the review of the actual earthquake response spectrum record, it

appears that the spectral acceleration at the frequency of interest for the measured

earthquake would result in exceeding the HCLPF capacity of the RWST.

Enclosure

50

The team conducted an independent walkdown of the RWST for Unit 1. Prior to

conducting the walkdown the team reviewed the walkdown inspection report conducted

by the licensee to identify areas of interest to the team. A licensee staff member

accompanied the team during the walkdown to address any questions the team had

related to the system. This inspection was focused on an assessment of the external

tank structure and foundation. The team observed the condition of the foundation pad

and weld and bolt anchor connections. One lose anchor bolt was identified by the

licensee and determined to exist prior to the seismic event. The licensee also identified

one area where grout under a base plate spalled but this was also determined to be

existing prior to the seismic event. The licensee was monitoring the tank level, (which

remained constant) for evidence of damage due to the seismic event. A review of

seismic calculations was conducted by the team to determine the structural design

margin. This review also included an evaluation of Dominion design drawing 11715-FV-

44A to verify structural elements and components are installed as designed. All walk-

downs for the RWST were completed during the time of inspection. The licensee was in

the process conducting testing to fully qualify this component.

Refueling Water Chemical Addition Tank

Per request of the team, the licensee provided information concerning how the tank was

connected to the support shroud. This information indicated that the 11/16 thick tank

shell was attached to the 5/8 thick support skirt via a 3/4 circumferential weld. A review

of licensees design drawing, 11715-FV-65A-4, Refueling Water Chemical Additional

Tank, identified a note that appeared to indicate that the tank was designed for a

horizontal acceleration of 1.84g and vertical acceleration of 1.23g. Table 3.2-1 of the

IPEEE report indicated a HCPLF of 0.19g. The team requested clarification of this

discrepancy. The licensee indicated that the basis for the acceleration values shown on

the drawing was not known. The inspectors reviewed licensees HCLPF calculation,

52308.04-C-005, Seismic Margin HCLPF Calculations for Refueling Water Chemical

Additional Tank, dated February 26, 1997. The calculation documented the basis of the

current HCLPF value of 0.19g for this tank. Based on the review of the actual

earthquake response spectrum record, it appeared that the measured earthquake would

result in exceeding the HCLPF capacity. The team performed a walkdown of the tank

and no significant issues were identified.

Internal Containment Structure

The containment consists of the concrete reactor building, its steel liner, and the

penetrations through this structure. The structure is designed to contain radioactive

material that may be released from the reactor core following a design basis LOCA.

Additionally, this structure provides shielding from the fission products that may be

present in the containment atmosphere following accident conditions.

The containment is a reinforced concrete structure with a cylindrical wall, a flat

foundation mat, and a hemispherical dome roof. The inside surface of the containment

is lined with a carbon steel liner to ensure a high degree of leak tightness during

operation and accident conditions. The concrete reactor building is required for

Enclosure

51

structural integrity of the containment under DBE conditions. The steel liner and its

penetrations establish the leakage limiting boundary of the containment.

The team conducted an independent walkdown of the interior of the containment

structure for both Unit 1 and Unit 2. Prior to conducting the walkdown the team reviewed

the walk-down inspection report conducted by the licensee to identify areas of interest to

the team. The licensee staff identified a through crack with minor spalling located in the

Unit 1 In-core RCP cubical wall. CRs 440252 and 440184 both documented this area

and this was inspected by the NRC team during the walkdown. A licensee staff member

accompanied the team during the walkdown to address any questions the team had

related to the containment. This inspection was focused on damage sustained by the

concrete structure, anchor bolts, and the exposed mat foundation, specifically cracks

and construction joint movement. The team inspected the foundation pad and weld and

bolt anchor connections. The team also reviewed the documentation associated with the

exterior of the Unit 1 containment. The team also reviewed Engineering Technical

Evaluations (ETE) conducted by the licensee through their ISI program before and after

the earthquake. This review also included an evaluation of design drawings to identify

areas of potential structural concern. All walkdowns for the Unit 1 containment were

completed during the time of inspection and licensee walkdowns for Unit 2 remained

ongoing during the time of the inspection observation.

Emergency Condensate Storage Tanks

During walkdowns, a puddle of liquid with brown stain was observed on the floor

adjacent to the tank. The team requested an explanation of the condition. The licensee

explained that the puddle was attributed to roof seal leakage and the condition was

documented in the licensees corrective action program prior to the earthquake as CR

376171. The team questioned whether the leak could be from the tank and the licensee

replied that there was no valve on the drain line from the tank enclosure to the catch

pan. After further investigation, the team concluded that this observation did not

represent a significant issue related to the earthquake since the condition was identified

prior to the earthquake.

Masonry Walls in Service Building

A crack was identified by the licensee on the Service Building masonry walls apparently

due to the earthquake. The team reviewed CR 439771 that addressed this issue. The

team performed a walkdown and no significant structural safety issues were identified.

8.3 Groundwater and Buried Pipe

a. Inspection Scope

The team reviewed the licensees processes and procedures established to control the

Buried Piping Monitoring/Ground Water Monitoring Program. The team reviewed

multiple documents and sampling data collected in response to the seismic event. The

team also conducted interviews with the licensee personnel involved in the response to

Enclosure

52

the seismic event. Finally, the team reviewed relevant/critical CRs developed during the

licensees post seismic assessment.

b. Observations and Findings

The licensee preformed an ETE on its Engineering Programs as a design input to

determine the impact of the seismic event. The Buried Pipe Monitoring/Ground Water

Monitoring Program was included in this ETE. The licensee conducted walkdowns of

numerous areas that were deemed risk-significant. The licensee routinely sampled

ground water on a quarterly basis but increased the planned frequency, inside the

stations Protected Area, to weekly for the first month after the event and then to monthly

for the next six months after that. The results of this increased sampling have not shown

any change in chemical levels tested within this program. It should also be noted that

during any significant liquid waste discharge such as releasing Boron Recovery Tank the

licensee is sampling on a daily basis. The team also conducted walkdowns of the

accessible portions of the Emergency Diesel Fuel Oil system and found no evidence of

leakage or damage.

9.0 Operability Determinations

a. Inspection Scope

To assess the adequacy of the licensees operability determinations for safety

equipment, the team performed the following activities:

  • Conducted walkdowns of the U1 and U2 EDGs and Main Steam Trip Valves; and

Unit 2 Pressurizer Power Operated Relief Valves (PORVs) to evaluate the material

condition

  • Conducted interviews with plant personnel (maintenance, engineering, and

operations) to establish a clear understanding of each system analysis

  • Reviewed design and engineering documents (i.e., calculations, drawings, vendor

manuals) to verify appropriateness of licensee actions in accordance with design and

licensing bases

  • Observed corrective maintenance and testing to assess the licensees actions to

restore the identified systems

In addition, the team reviewed corrective action CRs to evaluate the licensees response

to identified deficiencies associated with the identified systems. Completed work order

packages and test results were reviewed to verify the licensees restoration actions were

appropriately implemented and completed. Industry operating experience was

referenced to identify any potential generic industry issues.

The team also reviewed the recommendations that the licensee documented as follow-

up actions to the evaluation performed which included that the Fire Protection systems

be fully tested for each unit in accordance with RG 1.167 and concluded these were

appropriate actions prior to closing the functionality review.

Enclosure

53

b. Observations and Findings

Based on the scope of the inspection, no findings of significance were identified related

to licensee operability determinations.

Pressurizer PORVs

An OD was performed and documented in OD 000438 and 439, for the Pressurizer

PORVs to declare the valves operable but not fully qualified due to the possibility the

seismic accelerations experienced during the August 23 event may have exceeded a

portion of the applicable seismic response spectra used for the qualification of the

valves. Full qualification of the Pressurizer PORVs depended on completion of the

plants seismic review. The two Pressurizer PORVs on each unit were required in the

shutdown condition to relieve pressure, preventing any cold overpressure of the RCS.

The team reviewed the seismic calculations, which supported the licensees conclusion

that the valves were designed with margin to accept water hammer loads, followed by

steam in combination with the DBE seismic load. The team concluded that these

calculations validated the design margin of the valves, which was greater than the

seismic load alone. The team determined that these calculations in conjunction with the

visual walkdowns conducted by both the licensee and the inspection team, and the

functional performance testing performed on each units PORVs provided reasonable

assurance the valves could provide their design safety function.

1J & 2J EDG Jacket Water Cooling Pump Missing Orifice Plate

The team reviewed the OD written in response to the missing orifice discovered on the

1J and 2J EDGs. Section 5.0 of this report includes a more detailed discussion. The

team determined based on current parameters observed during testing, system

walkdowns, and engineering analysis, that the licensee supported their conclusion that

the EDGs could currently provide their design safety function.

Mode 5 and Mode 6 Systems

Two ODs were performed for systems required for Mode 5 and Mode 6, for both units,

and documented in OD 000442 (Mode 5 Systems) and OD 000448 (Mode 6 Systems).

The purpose of the ODs was to review the operability/functionality of systems required

by TS or the Technical Requirements Manual (TRM) for Mode 5 and Mode 6 following

the seismic event on August 23. The systems were declared Operable/Functional but

not fully qualified pending review and resolution of seismic issues.

The systems and components scoped in the Mode 5 OD included:

  • AC, DC, and Distribution Power Systems
  • EDGs and supporting systems (Start Instrumentation, Fuel Oil, Starting Air)

Enclosure

54

  • Boration Flow Path
  • ASME Code Class 1,2,3 Components
  • MOV Thermal Overload Protection Devices

The systems and components scoped in the Mode 6 OD were those needed to move the

units into a refueling condition and included, but not limited to:

  • Nuclear Instrumentation
  • Ventilation Systems
  • Spent Fuel Pool and supporting systems
  • Radiation Monitoring

The team reviewed the operability evaluations and concluded they were adequate in

determining the required systems were capable to perform their intended design

function; albeit, they were not fully qualified pending review of any seismic issues. The

operability determinations were based on successful completion of engineering

walkdowns and resolution of any discovered discrepancies; satisfactory completion of

functional testing; and engineering analysis of system performance.

During the review of the Mode 5 OD, the team noted that during the seismic event, minor

perturbations were observed on Units 1 and 2 RWST and SI accumulator levels. In

addition to these perturbations, other anomalies were noted to occur on various other

safety related instruments. Section 8.0 of this report includes additional discussion on

these perturbations.

Fire Protection & Appendix R Systems

A basis for functionality of the fire protection systems and Appendix R alternate

shutdown equipment was documented in a Reasonable Assurance of Safety (RAS)

review as RAS 000187. The RAS evaluation reviewed all aspects of the Fire Protection

and Appendix R systems (seismic and non-seismic) to determine reasonable assurance

they met their functional requirements without further compensatory actions.

The licensees review included functional validation of Appendix R systems including:

  • required instrumentation;
  • alternate shutdown equipment; and
  • equipment required to maintain communications.

Pumps and valves required for safe shutdown were operated and tested satisfactorily.

The Appendix R panels and isolations switches were installed safety-related and

seismically qualified and were inspected for damage and degradation and were found to

Enclosure

55

be available for service. The Appendix R radio channel, repeater, and antenna were

checked to perform their function satisfactorily. During containment walkdowns, the

reactor coolant pump oil collection systems were inspected and were found to have no

deficiencies.

Suppression systems for defense-in-depth were also verified and validated by the

licensee including:

  • Manual systems (i.e., extinguishers, hoses)
  • Detection systems (e.g., smoke and heat detectors)
  • Hydraulic systems (i.e., fire pumps, hydrants, standpipes)
  • Gaseous systems (e.g., CO2, halon)

On August 25, 2011, two days following the seismic event, a fire alarm for the Unit 2

reactor coolant pump 2-RC-P-1A radiant heat detector locked in and would not reset.

The license confirmed there was no fire present at the time of the alarm. The cause of

the alarm was not immediately identified; however, the team confirmed maintenance and

testing was being performed to determine the reason for the alarm. The team also

confirmed the licensee would inspect and test all circuits for the reactor coolant pump

heat detectors on both units prior to restarting.

Additionally, passive fire protection systems were visually inspected by the licensee for

any signs of degradation or damage as a result of the seismic event. This review

included a walkdown of structures including, but not limited to:

  • Fire doors;
  • Fire walls and barriers;
  • Penetration fire seals;
  • Radiant energy shields
  • Conduit fire wraps and seals

The licensees visual inspection identified some minor cracks in some of the fire walls

and barriers but determined they were only cosmetic in nature and did not constitute

degradation in barrier integrity given the cracks allowed no passage of air or light.

Based on the engineering walkdowns of the systems, results of applicable performance

tests and periodic maintenance, and use of the Test Requirements Manual to determine

functionality acceptance, the team concluded the licensee provided reasonable

assurance that the systems could meet their functional requirements; though, they would

be considered not fully qualified pending review of any applicable plant seismic issues.

The team reviewed the recommendations that the licensee documented as follow-up

actions to the evaluation performed, which included that the Fire Protection systems be

fully tested for each unit in accordance with RG 1.167 and concluded these were

appropriate actions prior to closing the RAS.

Enclosure

56

10.0 Restart Readiness

a. Inspection Scope

The inspectors conducted a review of the licensee plans and procedures for evaluating

the conditions of the plant prior to restart. At the close of the inspection, the licensee

had developed a plan for restart and presented the plan to the NRCs Office of Nuclear

Reactor Regulation for review.

b. Observations and Findings

Because the licensees restart plans were in development during most of the teams

inspection and because they were subject to separate NRC review, the team did not

draw conclusions related to the adequacy of the plans.

The licensees plan included nine parts, each of which detailed actions to be performed

prior to restart:

  • A characterization of the North Anna seismic event of August 23, 2011
  • Post-earthquake inspections of plant structures, systems, and components
  • Post-earthquake evaluation of reactor vessel internals
  • Post-earthquake assessment of new and irradiated fuel
  • Post-earthquake assessment of the spent fuel storage racks
  • Post-earthquake evaluation of the independent spent fuel storage installation
  • Post-earthquake impact assessment on engineering programs
  • Near-term actions to be completed prior to Unit startup
  • Long-term actions to be completed after Unit startup

The licensee planned to use the guidance of EPRI NP-6695, Guidelines for Nuclear

Plant Response to an Earthquake, dated 1989, which is endorsed by RG 1.167. At the

close of this inspection, the NRC was continuing to review the licensees plans.

Enclosure

57

11.0 Independent Spent Fuel Storage Installation (ISFSI)

a. Inspection Scope

The team reviewed design drawings associated with the two Independent Spent Fuel

Storage Installation (ISFSI) types contained in the storage area. In addition, the team

conducted a walkdown to assess the condition of each ISFSI pads and the associated

casks and the Horizontally Stored Modules (HSM) modules after the seismic event. The

team also conducted interviews with the licensee personnel involved in the response to

the seismic event. The seismic design methodology contained in FSAR was also

reviewed to determine the DBE for each type of ISFSI. Finally, the team reviewed all

CRs developed during the licensees post seismic assessment.

b. Observations and Findings

The team found that the ISFSIs were intact and found no significant damage during

walkdowns.

TN-32 Units (Pad 1)

There are two ISFSI pads at the North Anna site. Each pad supports two different types

of ISFSI units. ISFSI pad #1 stores TN-32. The TN-32 cask body is a right circular

cylinder composed of a confinement vessel with bolted lid closure, basket for fuel

assemblies, gamma shield, trunnions, neutron shield, overpressure monitoring system,

and a weather cover and is stored vertically on a 24 reinforced concrete pad supported

by an additional 48 of engineered backfill. The inspection team conducted a walkdown

of pad #1 to assess the condition of each of the ISFSI units. The team noted some

lateral sliding due to the seismic activity in 25 of the 27 TN-32 casks ranging from 0.5 to

4.5. As a result of this movement, six pair of the casks were found to be less than the

original minimum center to center spacing of 16 required by Section 4.0 of the TN-32

ISFSI Technical Specification. The team determined that the magnitude of sliding of TN-

32 casks was rather limited. The adjusted spacing based on movement due to the

earthquake ranged from 15-3.5 to 15-11. Section 4.0 of the TN-32 ISFSI TS also

states that space requirements are still in compliance based on 27.1 KW rating. The

licensee completed an Immediate OD for the ISFSI on August 23, 2011. All ISFSI

instrumentation was tested for operability and determined to be functioning properly. No

pressurization alarms were signaled during or after the seismic event. Based on a

review of the TN-32 ISFSI FSAR no sliding or tipping of the TN-32 casks is expected to

occur due to a DBE. Design drawings indicate the TN-32 casks are structurally

adequate to withstand the excitation of the earthquake as indicated by the pressurization

system alarm not tripping. No visual damage to the casks or the supporting pad was

observed by the inspection team.

The teams simplified analysis of ISFSI TN-32 casks subjected to the earthquake

shakings recorded at the Unit 1 Containment Basemat resulted in a factor of safety

against sliding greater than 1.0, indicating no sliding. A coefficient of friction between

the bottom of the steel casks and concrete pad of 0.3, as adopted in the FSAR, was

Enclosure

58

used in this analysis. Aside from the difference in subsurface conditions between the

Unit 1 and ISFSI sites and corresponding site soil amplifications, the team considered

that a potential deviation of the assumed value of 0.3 from the actual coefficient of

friction could be a contributing factor to the discrepancy between the analysis (no sliding)

and observation (sliding).

The teams inspection of the traces of sliding indicated that both the magnitude and

orientation of sliding were irregular across the pad. Casks on a surface-founded

concrete pad subjected to vertically propagating seismic waves are largely expected to

move uniformly across the pad based on the traditional assumption of coherent ground

motion. However, the irregular sliding pattern suggested to the team that the actual

ground motion at the ISFSI site might have been incoherent motion characterized by

spatial non-uniformity across the footprint of the pad. The team did not identify any

immediate safety concern associated with this observation or with the positioning of the

casks.

NUHOMS HD System (Pad 2)

The second ISFSI pad utilizes the NUHOMS HD-32PTH System, a horizontal canister

system composed of a steel Dry Shielded Canister (DSC) inside a reinforced concrete

Horizontal Storage Module (HSM-H). The NUHOMS HD is designed for enhanced heat

rejection capabilities, and permits storage of non fuel assembly hardware with the fuel

and/or damaged spent fuel assemblies. The welded DSC provides confinement and

criticality control for the storage and transfer of irradiated fuel. The concrete module

provides radiation shielding while allowing cooling of the DSC and fuel by natural

convection during storage.

The HSM-H is a reinforced concrete unit designed to provide environmental protection

and radiological shielding for the 32PTH DSC. The HSM-H consists of two separate

units: a base storage unit, where the 32PTH canister is stored, and a roof that serves to

provide environmental protection and radiation shielding. The roof is attached to the

base unit by four vertical ties or by four angle brackets. Three-foot thick shield walls are

installed behind each HSM-H (single row array only) and at the ends of each row to

provide additional environmental protection and radiological shielding. Each HSM-H

Unit has penetrations that are located at the top and bottom for air flow and are

protected from debris intrusions by wire mesh screens during storage operation. The

DSC Support Structure, a structural steel frame with rails, is installed within the HSM-H

module to provide for sliding the DSC in and out of the HSM-H and to support the DSC

within the HSM-H. HSM-Hs are arranged in arrays to minimize space and maximize

self-shielding.

The pad for these units is also 24 of reinforced concrete above 48 of engineered

backfill. These units were also walked-down by the inspection team in a similar manner.

The team noted minimal movement of these units during inspections of the roof and

ventilation system at the top of each unit. Based on post event inspections by the

licensee the HSM-H units have gaps between each module ranging from 0.5 to 1.5. It

should also be noted that 13 of the 26 NUHOMS HD Systems are loaded and the rest

Enclosure

59

are empty. The ventilation system for each HSM-H containing stored fuel within a DSC

was tested to determine if there was any blockage of airflow and it was determined that

each unit was functioning properly. The licensee had already documented exterior

damage caused by the seismic event.

Multiple areas of concrete spalling and cracking were identified by the licensee and

pointed out to the NRC team members during their walkdowns. All damage identified

was classified as cosmetic and the licensee determined each unit currently in service

was functioning properly. No damage to the supporting pad was observed by the

licensee or the NRC team members.

The main unknown related to both pads is the lack of seismic data for this area. No

seismic instrumentation was wired for this portion of the site. This area of the site was

approximately one half mile from the closest location seismic data was collected. This

makes it difficult to assess the performance of the area from a structural perspective.

Based on the information reviewed and the inspection activities conducted, the team

determined that there were no immediate safety concerns with the ISFSI facility.

12.0 Data for Risk Assessment

a. Inspection Scope

During the course of the inspection, the team collected information to support the final

determination of the risk of significance of the event. In accordance with Management

Directive (MD) 8.3, NRC Incident Investigation Program, deterministic and conditional

risk criteria were used to evaluate the level of NRC response for the operational event.

This issue met the deterministic criteria of MD 8.3 in that the ground movement of the

earthquake could have exceeded the design bases of the facility. The Conditional Core

Damage Probability (CCDP) for the event was estimated to be 1.1E-4.

b. Observations and Findings

Overall, the team concluded that the event did not adversely impact the health and

safety of the public. Safety limits were not approached and there was no measurable

release of radioactivity associated with the event.

The team collected additional information to support the NRCs final risk assessment.

The team noted that the CCDP estimate of 1.1E-4 relied, in part, on assumptions of

potential common cause aspects related to the failure of the 2H EDG due to a jacket

water leak about 45 minutes into the event. During the teams review of the 2H EDG

failure, the team determined that a faulty gasket installation in May 2010 may have

contributed to the EDGs failure and noted issues with the licensees maintenance

procedure that addressed gasket installation. An unresolved item was opened to

address the issue. Additional information on the 2H EDG failure may be found in

Section 5.0 of this report.

Enclosure

60

Additional issues with the EDGs were noted that could affect the NRCs final risk

assessment of the event. 1J EDG and 2J EDG were found to have missing orifice plates

in their jacket water cooling systems. At the time of the teams review, the licensee was

in the process of determining the significance of the missing orifice plates. An

unresolved item addressing this is described in Section 5.0. Also, while performing its

function during the event, 1J EDG experienced frequency oscillations that were

observed by operators in the control room. Reports from operators indicated that the

oscillations may have approached TS operability limits. At the time of the teams review,

the licensee had planned to test 1J EDG in isochronous mode. An unresolved item on

this issue is described in Section 6.0.

The team noted that the operators responded to the earthquake in accordance with

approved procedures and in a manner that protected public health and safety. Both

reactors automatically shut down during the event and safety system functions were

maintained. Plant walkdowns did not identify significant damage to the plant.

13.0 Safety Culture

a. Inspection Scope

Safety culture is defined as that assembly of characteristics and attitudes in

organizations and individuals, which establishes that, as an overriding priority, nuclear

plant safety issues receive the attention warranted by their significance. Therefore, an

organizations characteristics (i.e., safety culture components that comprise the visible

aspects of a safety culture) can be assessed by evaluating the extent to which its

policies, programs, and processes ensure that nuclear safety issues receive the

attention warranted by their significance. For example, the effectiveness of the

licensees corrective action program at identifying, prioritizing, and resolving issues with

nuclear safety impacts provides important insights into the licensees safety culture. An

organizations members shared attitudes and behaviors with respect to nuclear safety

also provide important insights into a licensees safety culture and can be assessed

through behavioral observations, interviews, and focus groups.

In conducting inspections to address the AIT charter items, the team interacted with and

interviewed licensee staff, reviewed corrective action program documents, and

examined licensee programs and policies. During this process, the team considered

safety culture components to determine whether safety culture was a contributing factor

in the event or issues related to the event.

b. Observations and Findings

No findings of significance were identified in this report related to the licensees safety

culture.

Enclosure

61

14.0 Exit Meeting Summary

On October 3, 2011, the NRC held a public meeting and presented the inspection results

to Mr. David Heacock and other members of the staff, who acknowledged the findings.

The inspectors asked the licensee whether any of the material examined during the

inspection should be considered proprietary. No proprietary information was identified.

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel:

W. Anthes, Manager, Nuclear Maintenance

M. Becker, Manager, Nuclear Outage and Planning

M. Crist, Plant Manager

R. Evans, Manager, Radiological Protection and Chemistry

T. Huber, Director, Nuclear Engineering

S. Hughes, Manager, Nuclear Operations

C. Gum, Manager, Nuclear Protection Services

L. Lane, Site Vice President

J. Leberstien, Technical Advisor Licensing

P. Kemp, Manager, Organizational Effectiveness

F. Mladen, Director, Station Safety and Licensing

R. Scanlon, Manager, Nuclear Site Services

D. Taylor, Supervisor, Station Licensing

R. Wesley, Manager, Nuclear Training

M. Whalen, Technical Advisor Licensing

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000338, 339/2011011-01 URI Seismic Instrumentation Implementation (Section 3.2)

05000338, 339/2011011-02 URI Failure of 2H Emergency Diesel Generator Jacket Water

Cooling Gasket Resulting in Inoperability during Dual Unit

LOOP (Section 5.0)

05000338, 339/2011011-03 URI Missing Orifice Plate on 1J and 2J EDG (Section 5.0)

05000338, 339/2011011-04 URI 1J EDG Frequency Oscillation (Section 6.0)

05000338, 339/2011011-05 URI Unit 1 Turbine Driven Auxiliary Feedwater Pump Trouble

Alarm (Section 7.1)

05000338, 339/2011011-06 URI Seismic Alarm Panel (Section 7.5)

05000338, 339/2011011-07 URI Safety Related Instrumentation Anomalies

(Section 8.1)

Discussed

None

Attachment 1

2

List of Documents Reviewed

Corrective Action Documents

CR 439724; VG-RI-178,179,180 seismic qualification; dated August 27, 2011

CR 439681; Determine which TR 3.3.6, TR 12.4 and TR section 7.0 SSC are seismic; dated

August 26, 2011

CR 439394; 2-RC-P-1A Radiant Heat Fire Alarm locked in; dated August 25 2011

CR 441362; 1-MS-TV-101B Train B SOV failed stroke time; dated September 4, 2011

CR 441358; 1-MS-TV-101A Train A SOV failed stroke time; dated September 4, 2011

CR 428754; Replace source range pulse shaper circuit card; dated May 26, 2011

CR 441864; Source range NI pulse shaper heat damage; dated September 7, 2011

CR 383161; Need a WO to change oil in the 2H EDG governor - revise cure time & installation

of water by-pass fitting; dated June 2, 2010

CR 440023; Incorrect torque values listed in procedures 0-MCM-0701-02/-27; dated August 29,

2011

CR 347658; Conflicting torque values on EDG water bypass plate fasteners; dated September

8, 2009

CR 347783; EDG water by-pass plates have incorrect surface finish; dated September 9, 2009

CR 442606; Standby Coolant Circulating Pump has 100 dpm seal leak; dated September 12,

2011

CR 439952; 2H EDG jacket cooling temperature dropped from 124 deg to 116 deg in 12 hrs;

dated August 28, 2011

CR 440297; 2H coolant leak; dated August 30, 2011

CR 439992; 2J EDG coolant water bypass connection inspection; dated August 28, 2011

CR 439091; 2H EDG manually secured; dated August 23, 2011

CR 439699; Generate new WO to inspect 2H EDG water bypass fitting gaskets

CR 440263; Torque water bypass fittings to 70 ft-lbs.; dated August 30, 2011

CR 439470; During start for Maintenance run, found 2H cylinder petcock valves open; dated

August 24, 2011

CR 439357; 2H EDG has an exhaust leak on OCS #4 extension pipe; dated August 25, 2011

CR 439272; Replace gaskets on 2H EDG; dated August 24, 2011

CR 439086; Generate WO to inspect 1J EDG; dated August 24, 2011

CR 439080; Generate WO to inspect 2J EDG; dated August 24, 2011

CR 439084; Generate WO to inspect 1H EDG; dated August 24, 2011

CR 439075; Generate WO to inspect 2H EDG; dated August 24, 2011

CR 439657; Perform OD for Unit 1 PORVs; dated August 26, 2011

CR 439662; Perform OD for Unit 2 PORVs; dated August 26, 2011

CR 441352; Engine driven coolant pump is leaking on 1J EDG; dated September 3, 2011

CR 441537; 1-EG-P-7J does not have an orifice plate installed on the discharge of the pump;

dated September 5, 2011

CR 441540; 2-EG-P-7J does not have an orifice plate installed on the discharge of the pump;

dated September 5, 2011

CR 440422; Request WO to repair coolant leaks identified during engine hydro; dated August

30, 2011

CR 439921; CR to allow processing of formal OD on ISFSI; August 28, 2011

CR 440205; Repair cosmetic concrete damage to NUHOMS HSM 1-3 intake vent; August 29,

2011

Attachment 1

3

CR 440207; Repair cosmetic concrete damage to NUHOMS HSM 23-25; August 29, 2011

CR 440204; Post seismic inspection found broken roof vent on HSM 15/17; August 29, 2011

CR 440200; Post seismic inspection of HSM 25 roof has cosmetic damage; August 29, 2011

CR 439315; ISFSI Pad 1 Post Seismic Inspection; August 24, 2011

CR 439319; ISFSI Pad 2 Seismic Inspection; August 24, 2011

CR 440987; ISFSI Pad 2 HSM Fastener; September 1, 2011

CR 440991; ISFSI Pad 1&2 Walkdown; September 1, 2011

CR 439921; CR to allow processing of formal OD on ISFSI; August 28, 2011

CR 440205; Repair cosmetic concrete damage to NUHOMS HSM 1-3 intake vent; August

29, 2011

CR 440207; Repair cosmetic concrete damage to NUHOMS HSM 23-25; August 29, 2011

CR 440204; Post seismic inspection found broken roof vent on HSM 15/17; August 29,

2011

CR 440200; Post seismic inspection of HSM 25 roof has cosmetic damage; August 29,

2011

CR 439315; ISFSI Pad 1 Post Seismic Inspection; August 24, 2011

CR 439319; ISFSI Pad 2 Seismic Inspection; August 24, 2011

CR 440987; ISFSI Pad 2 HSM Fastener; September 1, 2011

CR 440991; ISFSI Pad 1&2 Walkdown; September 1, 2011

CR 439217; Crack in Block Wall Above Door 1-BLD-STR-SO7-4 U2 307 Switchgear Back

Stairwell; dated August 23, 2011

CR 442328; Damage Found on C Phase CT Column for G202; dated September 10, 2011

CR 441027; Capacitor with Slight Bulge in 2H Swing Charger WU13 Card; dated September 1,

2011

CR 439210; 2J 4160V Relay Drops; dated August 24, 2011

CR 440227; Investigate Nuisance Alarms for Inverters while EDG Supplying Bus; dated August

23, 2011

CR 440231; Investigate 1-III and 1-IV Trouble Alarms while Energizing PZR Heaters; dated

August 23, 2011

CR 439127; 1-EP-SST-1A/1B Bus Duct Sagging - Previously Existing Condition; dated August

23, 2011

CR 439275; Unplanned Entry Into a Red Maintenance Rule Window; dated August 24, 2011

CR 439242; 2-EP-ST-2A1 No Mounting Bolts (Evaluate Before Energizing); dated August 23,

2011

CR 439204; Need Work Orders to Replace 500kV bushings on Unit 2 GSUs; dated August 23,

2011

CR 439202; Need Work Orders to Replace 500kV bushings on Unit 1 GSUs; dated August 23,

2011

CR 439194; PCS Points are Inaccurate for Unit 1G 4160V Bus; dated August 24, 2011

CR 439135; Breaker 01-EP-BKR-15G10 Fail to Close; dated August 24, 2011

CR 439306; 0-AP-23 Entered Due to Oil Leak within Berm of U1/U2 Main Transformers; dated

August 23, 2011

CR 439356; Line Fuse Clip Holder Installed in the Back of 1-EP-BKR-15C4 is Broken; dated

August 25, 2011

CR 439665; HI-Pot U2 Isophase; dated August 26, 2011

CR 439916; 2H1 Bus Potential Red Light Not Lit; dated August 28, 2011

Attachment 1

4

CR 439671; Programmatic Work Request U1 Isophase; dated August 29, 2011

CR 440145; Post Seismic Event System Engineering Walkdown - Emergency Switchgear

Room; dated August 29, 2011

CR 440164; Post seismic Event Walkdown - Insulation Falling from Top of 1-EI-CB 48B; dated

August 29;

CR 440068; Post Seismic Walkdown of the Vital Bus; dated August 29, 2011

CR 440065; Post Seismic Walkdown of Vital Bus; dated August 29, 2011

CR 439640; Walkdown of Unit 2 Cable Spreading Room Identified Broken Tie-Wraps; dated

August 26, 2011

CR 439638; Walkdown of Unit 1 Cable Spreading Room Identified Broken Tie-Wraps; dated

August 26, 2011

CR 440263; Torque Water Bypass Fittings to 70ft.lbs; dated August 30, 2011

CR 439812; Missing Vents on 1-EE-ST-1H; dated August 27, 2011

CR 442891; Recommended Revision to 0-AP-36, dated September 14, 2011

CR 212320; ETE-CEP-2011-0004, Update Underground Piping and Tank Life Cycle

Management (Unit 1); August 23, 2011

CR 212322; ETE-CEP-2011-0004, Update Underground Piping and Tank Life Cycle

Management (Unit 2); August 23, 2011

CR 439052; Event Review Team Issue Plan and Report for Dual Unit Trip Following Magnitude

5.8 Earthquake; dated September 3, 2011

CR 376171, NANN - Leakage from suction pipe gasket at U-1 ECST, 4-12-2010

CR 439771, NANN - Cracks in block north wall of service building locker room, 8-27-2011

Drawings

NAPS-S-ONE LINE; North Anna Power station Simplified One Line Diagram; Sh. 1; Rev. 1

11715-FE-1BB; One Line Diagram Electrical Distribution System; Sh. 1; Rev. 44

11715-FE-21P; D.C. Elementary Diagram Reserve Station Service Transformer Protection; Sh.

1; Rev. 8

11715-FE-5L-10; Wiring Diagram Rod Drive Supply Cabinet; Issue 10; Rev. D; dated March 18,

1988

11715-FE-21D1; D.C. Elementary Diagram Generator 1 and Transformers Protection; Sh. 1;

Rev. 2

11715-FE-1BD; One Line Switching Diagram Switchyard; Sh. 1; Rev. 44

11715/12050-1.30-201A; Emergency Diesel Generator Jacket Cooling Schematic; Rev. 5

11715-FM-070B; Flow/Valve Operating Numbers Diagram Main Steam Systems; Rev. 35

11715-TV-MS101A; Main Steam Line Trip Valve TV-MS101A Control; Sh. 1; Rev. 11

Transnuclear; DWG 10494-30-9, NUHOMS 32PTH, Transportable Canister for PWR Fuel

Basket Assembly, Rev 4

Transnuclear; DWG-NUH-03-7103; Base; Rev. 2

Transnuclear; DWG-NUH-03-7103; General Arrangement; Rev. 1

Transnuclear; DWG-NUH-03-7103; Roof, Rev. 2

Transnuclear; DWG-NUH-03-7103; Walls and Outlet Vent Cover; Rev. 2

Dominion, DWG-05004-0-1FC49A1; Plans, Section and Details ISFSI Storage; Rev. 3

Transnuclear, DWG-1049-30-1, TN-32 Dry Storage Cask Assembly and Parts (Longitudinal

Section); Rev. 12

Transnuclear; DWG-1049-30-2; TN-32 Dry Storage Cask Shell Assembly and, Rev. 15

Attachment 1

5

Transnuclear; DWG-1049-30-1; TN-32 Dry Storage Cask Overpressure Tank Assembly,

Rev. 12

12050-FW-157, Feedwater System Turbine Driven AUX FD Pump Lube Oil Reservoir Level

Switch & Alarm, Revision 33

122050-FE-1M, 480V One line Diag MCC 2A1-1, 2B1-2, 2C1-1 Above Cable Tunnel and MCC,

Revision XX

2A1-3 VAC Priming Hose North Anna Power Station Unit 2, Revision 33

12050-FE-1F, 480V One Line Diagram Bus 2A1, 2C2, 2B1, and 2A2, Revision 19

12050-FE-1B, 4160V One Line Diagram Bus 2A and Bus 2B North Anna Power Station Unit 2,

Revision 11

Drawing # 11715-FV-44A, Refueling Water Storage Tank, Rev. 7

Drawing # 11715-FV-65A-4, Refueling Water Chemical Additional Tank

Miscellaneous

Calculation # 52308.04-C-005; Seismic Margin HCLPF Calculations for Refueling Water

Chemical Additional Tank; dated February 26, 1997

Calculation # 52308.04-C-004; A-46 Evaluation of Refueling Water Storage Tank; Rev. 3; dated

March 15, 1999

Calculation # 52182-C-039, Seismic Margin HCLPF Calculations for Refueling Water Storage

Tank; Rev. 2; dated April 5, 1997

PO 70181906; VEPCO Power Transformer Standard Specifications

20497; Qualitrol 900/910 Series Rapid Pressure Rise Relay Operational Verification Test Report

Certification

20498; Qualitrol 900/910 Series Rapid Pressure Rise Relay Operational Verification Test Report

Certification

20499; Qualitrol 900/910 Series Rapid Pressure Rise Relay Operational Verification Test Report

Certification

Transformers Program/Component System Health Report; 3rd Quarter 2011

20110914T164920Z; Dissolved Gas Analysis; Transformer Oil Analyst 4.0; dated August 23,

2011

NAS-2027; Specification for Seismic Electrical Panels for Appendix R Isolation Panels; dated

March 7, 1985

QDR-N-8.5/QDR-S-8.3; Qualification Package for Rosemount 1153D Transmitter; Rev. 33

Rosemount Report D8300040; Qualification Report for Pressure Transmitters Rosemount

Model 1153 Series D; Rev. E; dated July 13, 2000

DC 94-016; SI Accumulator Level Transmitter Replacement

Quality Certificate of Compliance Data Sheet; Pressure Transmitter Rosemount Model

1152DP3N92PB; dated January 11, 1996

OE33510; Unit 1 NI Channel N32 Failed South Texas Project

NCRODP-23-NA; Main Steam System

Operator Logs

OD 000442; Prompt Operability Determination for Mode 5 systems; dated September 7, 2011

OD 000448; Prompt Operability Determination for Mode 6 systems; dated September 9, 2011

OD 000443/444; Prompt Operability Determination for 1J and 2J EDG missing orifice plates on

engine driven jacket water cooling pump; dated September 7, 2011

OD 000438/439; Prompt Operability Determination for Unit 1 and 2 PORVs; dated August 27,

2011

Attachment 1

6

RAS 000187; Reasonable Assurance of Safety Review of Appendix R Alternate Shutdown

Equipment; Rev. 1; dated September 9, 2011

14938-02-NPB-010-XC; Stress Analysis of Pressurizer Safety and Relief Piping (Class 1)

Reactor Containment; Rev. 0

CE-1109; Pipe Stress Analysis of PSARV Piping for DBE and SMA Spectra with Revised

Natural Frequency/Stiffness for Valves 1-RC-PCV-1455C and 1-RC-PCV-1456; Rev. 0

CE-1436; Seismic Qualification of Pressure Control Valves for USI A-46 and IPEEE; Rev. 0

ETE-NA-2011-0057; Evaluation 2H EDG Cooling Water Bypass Fitting Gasket Torque

Adequacy; Rev. 0

ETE-CEP-2011-0004; Impact of August, 2011Seismic Activity on Engineering Program; Rev.1

RP-AA-502; Ground Water Protection Program; Revision 2

EN#47181 - North Anna 1 & 2 - Alert Declared Due To An Earthquake In The Area And Loss Of

Offsite Power

EN#47196 - North Anna 1 & 2 - Unusual Event Declared Due To An Aftershock Earthquake

EN#47198 - North Anna 2 - Notification To Offsite Agency Regarding An Onsite Oil Spill

North Anna UFSAR, Revision 46.08, dated August 12, 2011

IEB 79-04; Incorrect Weights for Swing Check Valves Manufactured by Velan Engineering

Corporation; dated March 30, 1979

IEB 79-07; Seismic Stress Analysis of Safety-Related Piping; dated April 14, 1979

IEB 79-14; Seismic Analyses for As-Built Safety-Related Piping Systems; dated July 2, 1979

10 CFR 100, Appendix A, Seismic and Geologic Siting Criteria for Nuclear Power Plants

10 CFR 72.102, Geological and Seismology Characteristics

Regulatory Guide 1.100; Seismic Qualification of Electric and Mechanical

Equipment for Nuclear Power Plants, Revs.1 and 2

Regulatory Guide 1.92; Combining Model Responses and Spatial Components in Seismic

Response Analysis; Rev. 1

Regulatory Guide 1.60; Design Response Spectra for Seismic Design of Nuclear Power Plants,

Rev. 1

Regulatory Guide 1.61; Damping Values for Seismic Design of Nuclear Power Plants, Rev. 1

Regulatory Guide 1.97; Instrumentation for Light-Water-Cooled Nuclear Power Plants to A

Assess Plant and Environs Conditions During and Following an Accident; Rev.0

Regulatory Guide 1.166, Pre-Earthquake Planning and Immediate Nuclear Power Plant

Operator Post-Earthquake Actions; Rev. 1

Regulatory Guide 1.167, Restart of a Nuclear Power Plant Shutdown by a Seismic Event, Rev.

0

Regulatory Guide 1.13; Spent Fuel Storage Facility Design Basis; Rev. 1

Regulatory Guide 1.122; Development of Floor Design Response Spectra for Seismic Design of

Floor-Supported Equipment or Components; Rev. 1

Regulatory Guide 1.12; Nuclear Plant Instrumentation for Earthquakes; Rev. 1

NUREG-0800; Standard Review Plan for the Review of Safety Analysis Reports for Nuclear

Power Plants

USI A-46; Verification of Seismic Adequacy of Mechanical and Electrical Equipment in

Operating Reactors, dated February 27, 1987

NUREG-1742; Perspectives Gained from the Individual Plant Examination of External Events

(IPEEE) Program, Volume 1, Volume 2, dated April 2002

DCP-95-005; Independent Spent Fuel Storage Installation

Attachment 1

7

DCP 82-19; Spent Fuel Storage Racks

GL 87-02; Verification of Seismic Adequacy of Mechanical and Electrical Equipment in

Operating Reactors, Unresolved Safety Issue (USI) A-46, dated February 19, 1987

GL 88-20; Supplement 4, Individual Plant Examinations of Severe Accident Vulnerabilities,

dated June 28, 1991

GIP-2; Generic Implementation Procedure for Seismic Verification of Nuclear Plant

Equipment, Seismic Qualification Utility Group (SQUG), Revision 2, dated February 14, 1992

IEEE 344, IEEE Recommended Practice for Seismic Qualification of Class 1 E Equipment for

Nuclear Power Generating Stations, 1987 - 2004

STD-GN-0038; Seismic Qualification of Equipment, Rev. 9

STD-GN-0035, NRC Regulatory Guide 1.97 Compliance Engineering Guidelines for Post-

Accident Monitoring, Rev. 10

STD-CEN-001 6, Pipe Stress Analysis Standard for North Anna, Rev. 2

STD-CEN-0020, Equipment Supports - Mechanical & Electrical, Rev. 2

STD-CEN-0018, Nuclear Pipe Support Standard, Rev. 7

NAS-2016, Safety Related Standard for Conduit Supports, Rev. 8

NAS-0104, Design Criteria for Earthquake and Tornado Requirements for Structural Work,

Revision 3

Technical Report CE-0137, Seismic Event Abnormal Procedures and Seismic Instrumentation,

Revision 0

Technical Report PE-001 3, North Anna Power Station Response to Regulatory Guide 1.97,

Revision 14

NUREG-1407, Procedural and Submittal Guidance for the Individual Plant Examination of

External Events (IPEEE) for Severe Accident Vulnerabilities, dated June 1991

Letter VEPCO to Stone and Webster, Preliminary Report on Seismology, dated February 4,

1969

Letter Stone and Webster to VEPCO, Notes of Conference, dated August 27, 1969

Preliminary Safety Analysis Report, North Anna Power Station, dated March 1, 1969

NRC SER, Docket No. 50-338 and 50-339, Related to the Operation of North Anna Power

Station Units 1 and 2 (NUREG-0053), dated June 7, 1976

NRC SER, Docket No. 50-338 and 50-339, GL 87-02 Plant Specific Safety Evaluation for USI

Program Implementation at North Anna Power Station, Units 1 and 2, dated November 3,

2000

0-GEP-30, Post Seismic Event System Engineering Walk-down, Revision 2

NRC SSER No 2, Supplemental Safety Evaluation Report No. 2 (SSER No. 2) on Seismic

Qualification Utilities Group's Generic Implementation Procedure for Implementation of GL 87-

02 (USI A-46), Revision 2, corrected February 14, 1992,

Verification of Seismic Adequacy of Equipment in Older Operating Nuclear Plants, U.S. Nuclear

Regulatory Commission, dated May 22, 1992

NRC report to the Commission, Inquiry into Certain Issues Concerning the North Anna Fault

Matter, dated August 1978

DCP 78-18, Spent Fuel Racks

North Anna Power Station Units 1 & 2 Independent Spent Fuel Storage Installation (ISFSI)

Safety Analysis Report, Revision 2

NRC SER Issuance of Materials License SNM-2507 for the North Anna Independent Spent Fuel

Storage Installation, dated June 30 1998

Attachment 1

8

PDBD-NAPS, Plant Design Basis Document for North Anna Power Station, Revision 3, dated

April 19, 2011

North Anna Power Station Units 1 and 2 Report on Individual Plant Examination of External

Events (IPEEE) - Seismic, Prepared in Response to USNRC Generic Letter 88-20

Supplement 4 and 5, dated May 1997

North Anna, Units 1 and 2, Completion of Outlier Resolution - USI A-46 Program Generic Letter

(GL) 87-02 -- Verification of Seismic Adequacy of Mechanical and Electrical Equipment,

dated May 26, 2000

UFSAR Change Request NA-UCR-000-FN-1999-014, Seismic/Civil Integrated Review Team

(IRT) Change Package

Calculation 52308.04-0-003, USI A-46 Evaluation of Condensate Storage Tanks (CST) at North

Anna, Revision 1, dated April 9, 2007

EPRI Guideline NP-6695, Guidelines for Nuclear Plant Response to an earthquake, dated

January 26, 1990

Procedure VPAP-2802, Notifications and Reports, Revision 35, dated July 22, 2011

CR442891, Recommended Revision to 0-AP-36, dated September 14, 2011

CA212518, CA to North Anna Procedures to revise 0-AP-36 to verify detector, circuitry, and

Indication

VEPCO letter to the NRC, Response to the Request for Additional Information on Summary

Report on USI A-46 Program, Serial No.99-027, dated April 1 1999

Procedures

0-MCM-0701-27; Replacement of Emergency Diesel Generator Cylinder Liners; Rev. 19

0-MCM-0701-27; Replacement of Emergency Diesel Generator Cylinder Liners; Rev. 20

0-MCM-0701-27; Replacement of Emergency Diesel Generator Cylinder Liners; Rev. 21

2-OP-6.8; Slow Start and Operation of 2H Emergency Diesel Generator; Rev. 32

2-MOP-6.95; 2H EDG Coolant Changeout Using Bleed and Feed Method; Rev. 17

2-MOP-6.90; Emergency Diesel Generator 2-EE-EG-2H; Rev. 57

2-AR-17; Annunciator Response Procedure; Rev. 23

2-E-0; Reactor Trip or Safety Injection; Rev. 47

1-PT-36.9.1H; Degraded Voltage/Loss of Voltage Operational Test: 1H Bus; Rev. 11

Transformers - Operating Guidelines and Work Procedures; Electric Transmission and

Distribution Substations Operations and Maintenance; Rev. 1.0322011

05-04-06; FPR: 900, 910 Series; Control Operations Relay Test Procedures Manual; Rev. 3

1-EPM-1802-06; Protective Relay Maintenance for Reserve Station Service Transformer A

Differential and Backup Ground; Rev. 4

0-PT-39.1; Triaxial Time-History Accelerograph Instrument Channel Check; Rev. 7

1-PT-39.2; Triaxial Time-History Accelerograph Instrumentation and Seismic Operational Test;

Rev. 19

1-PT-39.8; Triaxial Time-History Accelerograph Calibration; Rev. 4; dated 10/25/2011

0-GEP-30; Post Seismic Event System Engineering Walkdown; Rev. 1

1-PT-212.29; Valve Inservice Inspection (1-RC-PCV-1455C) NDT Protection Response Time

Test; Rev. 9; dated August 24, 2011

1-PT-212.30; Valve Inservice Inspection (1-RC-PCV-1456) NDT Protection Response Time

Test; Rev. 9; dated August 24, 2011

2-PT-212.29; Valve Inservice Inspection (2-RC-PCV-2455C) NDT Protection Response Time

Test; Rev. 10; dated August 26, 2011

Attachment 1

9

2-PT-212.30; Valve Inservice Inspection (2-RC-PCV-2456) NDT Protection Response Time

Test; Rev. 10; dated August 26, 2011

2-PT-44.4.1; Overpressurization Protection Instrumentation Operational Test; Rev. 42; dated

August 25, 2011

1-PT-44.4.1; Overpressurization Protection Instrumentation Operational Test; Rev. 39; dated

August 25, 2011

1-PT-212.9; Valve Inservice Inspection (Main Steam); Rev. 17; Completed September 4, 2011

1-PT-36.8; Reactor Protection and Engineered Safety Feature Total Response Time

Verification; Rev. 32; dated September 7, 2011

0-AP-36; Seismic Event; Revision 19

0-PT-39.7; Seismic Instrumentation after a Seismic Event; Revision 3

1-E-0, Reactor Trip or Safety Injection, Revision 44

2-E-0, Reactor Trip of safety Injection, Revision 47

1-ES-0.1, Reactor Trip Response, Revision 30

2-ES-0.1, Reactor Trip Response, Revision 30

EPIP-1.01, Emergency Manager Controlling Procedure, Revision 46

EPIP-1.03, Response to Alert, Revision 18

2-AR-F-D8, 2-EI-CB-21F annunciator D8 Turbine Driven AFW Pump Trouble or Lube Oil

Trouble, Revision 2

Earthquake Response and the North Anna Restart Readiness Demonstration Plan during a

public meeting on September 8, 2011, ML11252A006

North Anna Power Station Emergency Plan, Rev. 36

NAPS Emergency Action Level Matrices (Hot and Cold) and Technical Bases Document,

Revision 2

EPIP-1.06, Protective Action Recommendations, Revision 9

EPIP-2.01, Notification of State and Local Governments, Revision 35

EPIP-3.02, Activation of Technical Support Center, Revision 30

EPIP-3.03, Activation of Operational Support Center, Revision 17

EPIP-4.01, Radiological Assessment Director Controlling Procedure, Revision 28

EPIP-4.02, Radiation Protection Supervisor Controlling Procedure, Revision 22

EPIP-4.05, Respiratory Protection and KI Assessment, Revision 10

EPIP-4.07, Protective Measures, Revision 19 and 20

0-AP-36, Seismic Event, Revision 19

0-AP-10, Loss of Electrical Power, Revision 67

0-AP-23, Oil or Hazardous Substance Spill Response, Revision 16

1-AP-22.1, Loss of 1-FW-P-2 Turbine-Driven AFW Pump, Revision 14

1-AP-19, Loss of Bearing Cooling Water, Revision 17

1-AP-28, Loss on Instrument Air, Revision 31

1-AP-33.1, Reactor Coolant Pump Seal Failure, Revision 15

1-AP-35, Loss of Containment Air Recirculation Cooling, Revision 18

1-AP-5, Unit 1 Radiation Monitoring System, Revision 33

2-AP-22.2, Loss of 2-FW-P-3A Motor-Driven AFW Pump, Revision 11

2-AP-19, Loss of Bearing Cooling Water, Revision 15

2-AP-13, Loss of One or More Circulating Water Pumps, Revision 17

2-AP-14, Low Condenser Vacuum, Revision 20

2-AP-35, Loss of Containment Air Recirculation Cooling, Revision 18

2-AP-5, Unit 2 Radiation Monitoring System, Revision 44

Attachment 1

10

Vendor Manuals

VTM 59-F173-00002; Fairbanks Morse Opposed Piston Engines Instructions 3800TD8-1/8

Model 38TD8-1/8 Diesel Stationary

ET-N-10-0054; Use of Inconel X-750 EDG Exhaust Gaskets; Rev. 0

00813-0100-4235; Rosemount 1152 Alphaline Nuclear Pressure Transmitter Data Sheet; Rev.

BA; dated April 2007

GEK-35003; General Electric Instruction Manual for Reserve Station Transformers

Qualitrol 900/910 RPRR; Rapid Pressure Rise Relays

59-K001-00004; Kinemetrics, Inc. Operating Instructions for Model SP-1/TS-3 Seismic Switch

System

59-K001-00005; Kinemetrics, Inc. FBA-3 Trixial Force-Balance Accelerometer; dated February

1, 1978

59-K001-00002; Kinemetrics, Inc. Operating Instructions for SMA-3 Strong Motion

Accelerograph System; dated August 8, 1976

59-K001-00001; Kinemetrics, Inc. Operating Instructions for Model TS-3 Triaxial Seismic

Switch; Rev. 1; dated June 1, 1989

VTM-59-M947-0003; GSU Transformer Replacement for Units 1&2 Transformers T4059

through T4066 512.5 - 22KV 400MVA Transformers; Rev. 1

Vendor Technical Manual 59-E01 5-00001, Model PAR400 Peak Acceleration Recorder

Operation and Maintenance Manual, Revision 2

Vendor Technical Manual 59-E015-00002, Model PSR 1200 Peak Shock Recorder Operation

and Maintenance Manual, Revision 2

Vendor Technical Manual 59-E015-00003, Models P5A875 and PSA1575 Peak Shock

Annunciator Operation and Maintenance Manual, Revision 1

Vendor Technical Manual 59-K001-00001, Operating Instructions for SMP-1 Magnetic Tape

Playback System, Revision 1

Vendor Technical Manual 59-K001-00002, Operating Instructions for SMA-3 Strong Motion

Accelerograph System, Revision 2

Vendor Technical Manual 59-K000-00003, Operating Instructions for Model TS-3 TriaxaI

Seismic Switch, Revision 1

Vendor Technical Manual 59-K001-00004, Operating Instructions for Model SP-1/TS-3 Seismic

Switch System, Revision 1

Vendor Technical Manual 59-K001-00005 Operating Instructions for FBA-3 Triaxial Forced-

Balance Accelerometer, Revision 1

Work Orders

WO 59102038161; 2H EDG Install New Style Oil Scraper Rings and Pistons; dated May 27,

2010

WO 59080512401; 1H EDG Replace All 12 Cylinder Liners; dated September 9, 2009

WO 59079496201; 1J EDG Replace 10 Remaining Old Style Cylinder Liners; dated September

17, 2009

WO 59101704113; 2J EDG Replace All 12 Cylinder Liners; dated January 16, 2011

WO 59102341733; 2H EDG Repair Coolant Leak Post EPIP-3.03 Documentation; dated August

23, 2011

WO 59102342316; 2H EDG Replace Exhaust Gasket OCS #4 Extension Pipe; dated August,

25, 2011

WO 59102342452; 2H EDG Replace Water Inlet Gaskets on CS; dated August, 30, 2011

Attachment 1

11

WO 59102344717; 2J EDG Replace Water Inlet Pipe Gaskets; dated September 1, 2011

WO 59102341713; 2H EDG Remove Heat Shields For Inspection; dated August 24, 2011

WO 59102341714; 2J EDG Remove Heat Shields For Inspection; dated August 28, 2011

WO 59102341715; 1H EDG Remove Heat Shields For Inspection; dated August 28, 2011

WO 59102341716; 1J EDG Remove Heat Shields For Inspection; dated 8/xx/11

WO 59102345583; 1H EDG Water Bypass Fittings Re-Torque; dated September 2, 2011

WO 59102345639; 1J EDG Water Bypass Fittings Re-Torque (CS/OCS); dated September 3,

2011

WO 59102349576; Rebuild/Replace Coolant Pump on 1J EDG; dated September 5, 2011

WO 59102346517; Crane #15 Possible Bus Bar Damage; dated September 7, 2011

WO 59101674310; Protective Relay Maintenance for Reserve Station Service Transformer A

Differential and Backup Ground; Rev. 4; dated July 27, 2009

WO 59102343487; Perform Hi-pot Test for the U1 Isophase Bus Duct (Post Seismic

Inspection); dated August 31, 2011

WO 59102343486; Hi-Pot U2 Isophase; dated August 31, 2011

WO 59102345224; Post Seismic Event Walkdown - Fuse Holder 1-EI-CB-48B Found in Bottom

of Cabinet, dated August 31, 2011

WO 59102342521; 2J 4160V Relay drops; dated August 31, 2011

Attachment 1

SEQUENCE OF EVENTS

North Anna Power Station, Unit 1

Date/Time Event Description

August 23, 2011 Unit 1 at 100% power; U1 Turbine Driven Auxiliary Feedwater pump

removed from service for scheduled surveillance test

Magnitude 5.8 earthquake with epicenter near Mineral VA

13:51:10.224 Pressurizer High Level, Back up Heaters alarm begins to toggle. This is

assumed to be the onset of the earthquake on Unit 1

13:51:11.722 Power Range Instrument High Flux Rate (N42) received

13:51:11.791 Reactor Coolant System Loop 1A Low Flow Channel III alarm begins to

toggle

13:51:11.867 Power Range Instrument High Flux rate (N41) received

13:51:11.873 Nuclear Instruments Power Range High Flux Rate Trip Reactor Trip is

the first Out Reactor Trip signal

13:51:11.888 Main Transformer Sudden Pressure Relay (63X ABC) received

13:51:11.892 Main Transformer Low Relay Turbine Trip (86T) is the First Out Turbine

Trip Signal

13:51:11.918 B Reactor Trip Breaker Open

13:51.11.927 A Reactor Trip Breaker Open

13:51.12.047 Reserve Station Service Transformer B Sudden Pressure Relay (63A)

alarm received. B Reserve Service Transformer is de-energized

13:51:12.055 Generator output Breaker open (G12)

13:51:12.058 Reserve Station Service Transformer A Sudden Pressure Relay (63A)

alarm received. A Reserve Station Service transformer is de-energized

13:51:12.558 Reserve Station Service Transformer C Sudden Pressure Relay (63A)

alarm received. C Reserve Station Service Transformer is de-energized

13:51:12.695 Rod Position Indicator Rod Bottom Rod Drop received. Rods inserted.

Attachment 2

SEQUENCE OF EVENTS

North Anna Power Station, Unit 1

August 23, 2011 (continued)

Date/Time Event Description

13:51:13.384 Motor Driven Auxiliary Feedwater Pumps supplying B and C Steam

Generators. Steam Driven Pump Performance Test was in progress prior

to the event

13:51:15.570 Motor Driven Auxiliary Feedwater Pumps shut down on Emergency bus

undervoltage

13:51:20.579 1J Re-energized from 1-EE-EG-1J (1J Emergency Diesel Generator)

13:51:21.590 B Motor Driven Auxiliary Feedwater Pump re-started

13:51:21.669 1H Re-energized from 1-EE-EG-1H (1H Emergency Diesel Generator)

13:51:22.650 A Motor Driven Auxiliary Feedwater pump re-started

Attachment 2

SEQUENCE OF EVENTS

North Anna Power Station, Unit 2

Date/Time Event Description

August 23, 2011 Unit 2 at 100% power

Magnitude 5.8 earthquake with epicenter near Mineral VA

13:51:11.072 Refueling Water Storage Tank Chemical Addition Tank Low Level On

alarm begins to toggle. This is assumed to be the onset of the earthquake

on Unit 2

13:51:11.559 Pressure High Level Back Up Heaters On alarm begins to toggle similar

to Unit 1.

13:51:11.676 Power Range Instrument High Flux Rate (N41) received

13:51:11.756 Reactor Coolant System Loop A Channel I Low Flow alarm begins to

toggle

13:51:11.768 Reactor Coolant System Loop B Channel II Low Flow alarm begins to

toggle

13:51:11.829 Power Range Instrument High Flux Rate (N42) received

13:51:11.829 Power Range Instrument High Flux Rate (NI) Reactor Trip is the first

Out Reactor Trip signal

13:51:11.860 Reactor Coolant System Loop C Channel III Low Flow alarm begins to

toggle

13:51.11.888 A Reactor Trip Breaker Open

13:51.11.891 B Reactor Trip Breaker Open

13:51.11.900 Reactor Tripped - Turbine Trip is the first Out Turbine Trip signal

13:51:11.969 Main Transformer Low Relay Turbine Trip (86T) alarm received

13:51:12.048 Main Transformer Sudden Pressure Relay (63A) alarm received. B

Reserve Station Service Transformer is de-energized.

13:51:12.059 Main Transformer Sudden Pressure Relay (63A) alarm received. A

Reserve Station Service Transformer is de-energized.

13:51:12.193 Rod Position Indicator Rob Bottom Rod Drop received. Rods inserted.

Attachment 2

SEQUENCE OF EVENTS

North Anna Power Station, Unit 2

August 23, 2011 (continued)

Date/Time Event Description

13:51.12.559 Reserve Station Service Transformer C Sudden Pressure Relay (63A)

alarm received. C Reserve Station Service transformer is de-energized

13:51:14.139 All Auxiliary Feedwater Pumps running and supplying respective Steam

Generators

13:51:16.260 Motor Driven Auxiliary Feedwater Pumps shut down on Emergency bus

undervoltage

13:51:20.196 2H Re-energized from 2-EE-EG-2H (2H Emergency Diesel Generator)

13:51:21.100 A Motor Driven Auxiliary Feedwater Pump re-started

13:51:21.296 2J Re-energized from 2-EE-EG-2J (2J Emergency Diesel Generator)

13:51:22.130 B Motor Driven Auxiliary Feedwater pump re-started

Attachment 2

SEQUENCE OF EVENTS

North Anna Power Station, Unit 1 and 2

August 23, 2011 Unit 1 and Unit 2 in Mode 3

Date/Time Event Description

14:03 Alert declared Tab HA6.1, Shift Manager judgment

14:19 1-FW-P-2 available (flowing to A Steam Generator)

14:40 2H Emergency Diesel Generator manually tripped on coolant leak 2H

Emergency Bus de-energized

14:55 Alert declared Tab SA1.1 U2 AC capability reduced to a single source

(2J Emergency Diesel Generator)

15:18 2H Emergency Bus de-energized by the Station Blackout Diesel

17:23 Energized C Reserve Station Service Transformer and F transfer bus

17:40 2J emergency bus transferred to C Reserve Station Service

Transformer

17:48 1H energized from F transfer bus, securing 1H Emergency Diesel

Generator

20:03 B Reserve Station Service Transformer energized

20:17 A Reserve Station Service Transformer energized

22:58 Offsite power supplying Emergency Busses, 3 Emergency Diesel

Generators and Station Blackout diesel is Auto and available

August 24, 2011

08:51 Commenced Unit 1 cooldown

11:16 Downgrade to Notice of Unusual Event under Tab HU1.1

13:15 Notice of Unusual Event terminated

13:34 Unit 1 in Mode 4, Hot Shutdown

21:26 Unit 1 in Mode 5, Cold Shutdown

Attachment 2

SEQUENCE OF EVENTS

North Anna Power Station, Unit 1 and 2

Date/Time Event Description

August 25, 2011

01:08 Notice of Unusual Event declared under tab HU1.1 (aftershock)

11:37 Commenced Unit 2 cooldown

16:22 Unit 2 in Mode 4, Hot Shutdown

August 26, 2011

14:05 NRC notification emergency preparedness criteria seismic activity >

Operating Basis Earthquake met but not declared (Emergency Action

Level HAA6.1 versus HA1.1)

16:23 NRC notification of potential unanalyzed condition (Design Basis

Earthquake above 5 Hz)

20:38 Unit 2 in Mode 5, Cold Shutdown

August 28, 2011

15:36 Notice of Unusual Event terminated

September 1, 2011

05:18 Notice of Unusual Event declared, Tab HU1.1 (aftershock)

12:23 Notice of Unusual Event terminated

Attachment 2

Attachment 3

Attachment 3

Attachment 3

Attachment 3

Attachment 3

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4

Attachment 4