IR 05000338/2021013

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Biennial Problem Identification and Resolution Inspection Report 05000338/2021013 and 05000339/2021013
ML21286A700
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 10/13/2021
From: Stewart Bailey
NRC/RGN-II
To: Stoddard D
Virginia Electric & Power Co (VEPCO)
References
IR 2021013
Download: ML21286A700 (15)


Text

October 13, 2021

SUBJECT:

NORTH ANNA POWER STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000338/2021013 AND 05000339/2021013

Dear Mr. Stoddard:

On September 3, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your North Anna Power Station and discussed the results of this inspection with Mr. Fred Mladen and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

One finding of very low safety significance (Green) is documented in this report. This finding did not involve a violation of NRC requirements. If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at North Anna Power Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Stewart N. Bailey, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos. 05000338 and 05000339 License Nos. NPF-4 and NPF-7

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000338 and 05000339 License Numbers: NPF-4 and NPF-7 Report Numbers: 05000338/2021013 and 05000339/2021013 Enterprise Identifier: I-2021-013-0003 Licensee: Virginia Electric and Power Company Facility: North Anna Power Station Location: Mineral, VA Inspection Dates: August 16, 2021 to September 03, 2021 Inspectors: D. Mas-Penaranda, Resident Inspector L. McKown, Senior Resident Inspector M. Schwieg, Senior Reactor Inspector J. Seat, Senior Project Engineer Approved By: Stewart N. Bailey, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at North Anna Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Condition Monitoring Inspection Failure of Unit 1 Main Condenser Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green [H.14] - 71152B FIN 05000338/2021013-01 Conservative Open/Closed Bias A self-revealed Green finding was identified when the licensee failed to provide sufficient instruction and support in accordance with the self-imposed standard established in 0-NSP-CN-001, Inspection of the Main Condenser, Rev. 0. Specifically, an inadequate inspection resulted in the failure to identify adverse conditions associated with cyclic fatigue at the 1-SD-TK-2A, high level divert line and branch connection end cap within the North Anna Power Station Unit 1 main steam surface condenser which in turn resulted in component failure, loss of condenser vacuum, and a reactor trip on May 7, 2021.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000338/2021-001-00 LER 2021-001-00 for North 71153 Closed Anna Power Station, Unit 1,

Manual Reactor Trip on Degrading Condenser Vacuum Due to Piping Failure

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), inspectors were directed to begin telework. In addition, regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program (CAP), use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted an in-depth CAP review of the high head safety injection system, auxiliary feedwater system and emergency diesel generators.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Follow Up (IP Section 03.01)

(1) LER 05000338/2021-001-00, North Anna Power Station, Unit 1, Manual Reactor Trip on Degrading Condenser Vacuum Due to Piping Failure (ADAMS Accession No. ML21195A186). The inspection conclusions associated with this LER are documented in this report under Inspection Results Section.

INSPECTION RESULTS

Assessment 71152B 1. Corrective Action Program Effectiveness Problem Identification: The team determined that the licensee was effective in identifying problems and entering them into the corrective action program and that there was a low threshold for entering issues into the corrective action program. This conclusion was based on a review of the requirements for initiating condition reports as described in licensee procedure PI-AA-200, "Corrective Action," and managements expectation that employees were encouraged to initiate condition reports. Additionally, site management was actively involved in the corrective action program and focused appropriate attention on significant plant issues.

Problem Prioritization and Evaluation: Based on the review of condition reports, the team concluded that problems were prioritized and evaluated in accordance with the condition report significance determination guidance in procedure PI-AA-200. The team determined that adequate consideration was given to system or component operability and associated plant risk. The team determined that plant personnel had conducted cause evaluations in compliance with the licensees corrective action program procedures and that cause determinations were appropriate, and considered the significance of the issues being evaluated.

Corrective Actions: Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the team determined that corrective actions were mostly timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence. The team reviewed condition reports and effectiveness reviews to verify that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence were sufficient to ensure corrective actions were properly implemented and were effective.

Based on the samples reviewed, the team determined that the licensees corrective action program complied with regulatory requirements and self-imposed standards. The licensees implementation of the corrective action program adequately supported nuclear safety.

2. Operating Experience The team determined that the station's processes for the use of industry and NRC operating experience information and for the performance of audits and self-assessments were effective and complied with all regulatory requirements and licensee standards. The implementation of these programs adequately supported nuclear safety. The team concluded that operating experience was adequately evaluated for applicability and that appropriate actions were implemented to address lessons learned as needed.

3. Self-Assessments and Audits The team determined that the licensee effectively performs self-assessments and audits to identify issues at a low level, properly evaluated those issues, and resolved them commensurate with their safety significance.

Self-assessments were generally detailed and critical. The team verified that condition reports (CRs) were created to document areas for improvement and findings resulting from self-assessments and verified that actions had been completed consistent with those recommendations. Audits of the quality assurance program appropriately assessed performance and identified areas for improvement. Generally, the licensee performed evaluations that were technically accurate.

4. Safety Conscious Work Environment

Based on interviews with plant staff and reviews of the latest safety culture survey results to assess the safety conscious work environment on site, the team found no evidence of challenges to the safety conscious work environment. Employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

Condition Monitoring Inspection Failure of Unit 1 Main Condenser Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green [H.14] - 71152B FIN 05000338/2021013-01 Conservative Open/Closed Bias A self-revealed Green finding was identified when the licensee failed to provide sufficient instruction and support in accordance with the self-imposed standard established in 0-NSP-CN-001, Inspection of the Main Condenser, Rev. 0. Specifically, an inadequate inspection resulted in the failure to identify adverse conditions associated with cyclic fatigue at the 1-SD-TK-2A, high level divert line and branch connection end cap within the North Anna Power Station Unit 1 main steam surface condenser which in turn resulted in component failure, loss of condenser vacuum, and a reactor trip on May 7, 2021.

Description:

On May 7, 2021, with down power in progress following identification of exceedance of Chemistry Specification CH-99.600, secondary chemistry action level 3, operators manually tripped North Anna Power Station Unit 1 from 60 percent rated thermal power due to degrading condenser vacuum. Dominion Energy determined that high cycle fatigue piping failure of the A high pressure heater drain receiver high level divert line caused damage to condenser tubes, resulting in the rapid degradation of secondary chemistry and vacuum.

The licensee performed material analysis of the piping failure location within the Unit 1 main condenser. The opened crack fracture surfaces displayed mixed morphologies. In most areas, particularly at the branch connection welds, the surfaces were either worn, eroded, corroded, or a combination of all three. This indicates that the cracking in these areas was not a single recent event but had initiated years ago along the outside of the weld. The licensee also observed breach marks on portions of the fractures. This further supports that the cracking was associated with fatigue failure that developed over time from variable loading conditions. Moreover, the material analysis found that the weld quality was poor at multiple locations. The welds appeared to be undersized and showed a lack of weld penetration. This resulted in LER 05000338/2021-001-00, North Anna Power Station, Unit 1, Manual Reactor Trip on Degrading Condenser Vacuum Due to Piping Failure (ADAMS Accession No. ML21195A186).

North Anna Power Station performs condition monitoring of the main condensers via complete visual inspection in accordance with 0-NSP-CN-001, Inspection of the Main Condenser. This activity is performed every 36 months by engineering staff qualified to perform condition monitoring in accordance with the station aging management program. The licensee found that previous inspection of the failure location had been satisfied by performing an eyes only visual inspection from a walking surface, feet above, the area. Prior to the event, this methodology was determined adequate for identifying gross degradation.

However, the lack of detailed inspection allowed fatigue cracking to propagate over multiple operating cycles until the piping failed and damaged condenser tubes.

Corrective Actions: The station has established corrective actions to improve the procedural guidance within 0-NSP-CN-001, providing greater detail on inspection methodology, enhancing component access via scaffolding, and incorporating technology and industry best practices.

Corrective Action References: CA8477763

Performance Assessment:

Performance Deficiency: The inspectors found that Dominion Energy's failure to provide sufficient instruction and support in accordance with the self-imposed standard established in 0-NSP-CN-001, resulting in unidentified fatigue damage and a reactor trip, was a performance deficiency reasonably within the licensee's ability to foresee and prevent.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Procedure Quality attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, procedure 0-NSP-CN-001 lacked adequate steps to perform visual inspection of the Unit 1 main steam surface condenser. This resulted in the failure to identify adverse conditions, which based upon the licensee's material evaluation, persisted for multiple cycles of inspection, leading to equipment failure and a reactor trip. The inspectors used IMC 0612, Appendix E, Examples of Minor Issues, dated January 1, 2021, to inform answers to the more than minor screening questions and found this condition consistent with more than minor example 4.b.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. In accordance with Exhibit 1, Initiating Events Screening Questions, B. Transient Initiators, this event screens to Green as following the trip operators stabilized condenser vacuum to maintain functionality through unit recovery.

Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. The licensee did not take a conservative approach to decision making associated with inspection of the Unit 1 main steam surface condenser, particularly when performing eyes only visual inspection of cyclically stressed components from feet away.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On September 3, 2021, the inspectors presented the biennial problem identification and resolution inspection results to Mr. Fred Mladen and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71152B ALARA Plans21-003 NUHOMs EOS Cask Loading Campaign 0

21-003 NUHOMs EOS Cask Loading Campaign 1

21-003-001 Work In Progress ALARA Review 0

Corrective Action 1141471 Condition Reports

Documents 1124204

26153

27484

28095

28297

29617

1132180

1134248

1138540

1136938

1141532

1142054

1149745

1150309

1150509

1151692

1151719

1154837

1158144

1158244

1161082

1161318

1161363

1164662

1165578

1165793

1168559

1168720

Inspection Type Designation Description or Title Revision or

Procedure Date

1169129

1170953

1174843

29636, 533999, Condition Reports associated with Chemical and Volume

545489, 575536, Control System Work Request Tags

1011453,

1041183,

1041253,

1041402,

1041404,

1045981,

1054538,

1055192,

1060920,

1065357,

1065648,

1086171,

1086583,

1087121,

1087123,

1093954,

1108169,

1109238,

1110259,

20669,

20670,

29404,

1141757,

1141866,

1153283,

1164943,

1174426,

1174644,

1177293,

Inspection Type Designation Description or Title Revision or

Procedure Date

1177300

236171 Corrective Actions

7876917

CA7932524

CA8477763

CR1138179

CR1165443

CR1137734

CR1135934

CR1132150

CR1129761

CR1178405

LEE CA 7784888 U1 Terry Turbine MS Drain Line repairs

Corrective Action CR1103946,

Documents CR1178860,

Resulting from CR1178894,

Inspection CR1178935,

CR1179833,

CR1179930,

PA8567395

Engineering LEE CR1144530 Pressure Boundary Leak on Unit 2 "A" RCP Seal Injection Line 0

Evaluations LEE CR458189 Diesel Driven Fire Pump failure 0

PIR1140204 OE#465752 Surry Fire Main Rupture 0

PIR1141381 OE469857R20200213 Unattended Locked High Radiation 0

Area

PIR1146037 OE454908R20200430 Heater Drain Pump Motor Fire and 0

Declaration of Unusual Event

PIR1149770 OE475066R20200612 Unposted Locked High Radiation Area 0

Created in Drywell Subpile Room

PIR1150164 OE458344R20200619 Postulated Hot Short from DC Control 0

Circuits Through Safe Shutdown Fire Protect

PIR1166359 PART 21 - Limitorque Actuator Fatigue 0

Miscellaneous Emergency Diesel Generator System Monitoring Plan

Requirements

Inspection Type Designation Description or Title Revision or

Procedure Date

Emergency Diesel Generator System Health Report, 2020 4th 06/15/2021

Quarter

LER 50-338/2021- Manual Reactor Trip on Degrading Condenser Vacuum Due to

001-00 Piping Failure

(ML21195A186)

VTM 59-C550- Cummins NT-280-IF water cooled engines 4

00001

Operability Analysis of 01-EE-EG-1J, Emergency Diesel Generator No. 1 03/13/2020

Evaluations Cylinder Piston Pin Bushing Degradation and Past Operability

CA8524213

CR1129761 SW MOVs HBC-0 Qualified Stroke Count Exceeded 0

CR1132150 The licensing basis and design basis for the Equipment hatch 0

platform are not aligned.

CR1137734 MOV weak link not accurately modeling QSS stem cuts 0

CR1165443 X-QS-MOV-X01 A/B Control Logic Results in Potential 0

Negative Design Margin

Procedures 0-MCM-1801-01 WELDING SAFETY-RELATED AND SEISMIC-RELATED 30

EQUIPMENT

0-MPM-01 07-01 DIESEL FIRE PUMP PREVENTIVE MAINTENANCE 20

0-NSP-CN-001 Inspection of the Main Condenser 0

1-PT-83.12H/J, Diesel Generator Test (Start by ESF Actuation) Followed by Rev. 33/34

1H/J 24-Hour Run and Hot Restart Test

2-PT-83.12H/J, Diesel Generator Test (Start by ESF Actuation) Followed by Rev. 35/36

2H/J 24-Hour Run and Hot Restart Test,

ER-AA-101 System Engineering Walkdowns 5

MS-AA-WHS-133 In-Storage Maintenance of Items 6

PI-AA-100-1007 Operating Experience Program 7

RP-AA-300 ALARA Reviews and Reports 10

Work Orders 59203355106

59102676139

203137149

203267789

59103099207

203324709

Inspection Type Designation Description or Title Revision or

Procedure Date

203282506

203294676

203323891

203301735

203293580

203302577

203302579

203302580

WO 59203356197

2