ML110610641

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NRC Report 05000259/2010005, 05000260/2010005, and 05000296/2010005; Preliminary Greater than Green Finding Browns Ferry Nuclear Plant
ML110610641
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 03/02/2011
From: Croteau R
Division Reactor Projects II
To: Krich R
Tennessee Valley Authority
References
EA-11-012, EA-11-018 IR-10-005
Download: ML110610641 (70)


See also: IR 05000259/2010005

Text

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

March 2, 2011

EA-11-018

Mr. R. M. Krich

Vice President, Nuclear Licensing

Tennessee Valley Authority

1101 Market Street, LP 3R-C

Chattanooga, TN 37402-2801

SUBJECT: NRC REPORT 05000259/2010005, 05000260/2010005, AND

05000296/2010005; PRELIMINARY GREATER THAN GREEN FINDING

BROWNS FERRY NUCLEAR PLANT

Dear Mr. Krich:

This letter discusses a finding that has preliminarily been determined to be Greater than Green,

that is, a finding of greater than very low safety significance resulting in the need for further

evaluation to determine significance and therefore the need for additional NRC action. This

finding involves the failure to establish adequate design control and perform adequate

maintenance on the Unit 1 low pressure coolant injection (LPCI) outboard injection valve,

1-FCV-74-66, resulting in the valve being left in a significantly degraded condition and residual

heat removal (RHR) loop II unable to fulfill its safety function. This finding was assessed based

on the best available information, using the applicable Significance Determination Process

(SDP) and was calculated to have a preliminary conditional core damage probability of 7.3E-4.

A factor that may reduce the preliminary probability result includes a reduction in the period of

exposure time that the valve was in a failed condition. In addition, the ability to maintain reactor

water levels and core cooling through the valve or by other sources may also reduce the

preliminary probability. The final resolution of this finding will be conveyed in separate

correspondence.

This finding was considered more than minor because it was associated with the Protection

Against External Factors attribute of the Reactor Safety/ Mitigating Systems Cornerstone and

adversely affected the cornerstone objective of ensuring availability and reliability of systems

designed to respond to initiating events to prevent undesirable consequences. Specifically, the

RHR loop II subsystem was rendered incapable of being aligned to perform its safe shutdown

function due to the failure of 1-FCV-74-66. Fire risk dominates the impact of this equipment

failure finding. Tennessee Valley Authoritys method for severe fire mitigation at Browns Ferry

implements a strategy that includes actions that procedurally de-energize all Emergency Core

Cooling System (ECCS) equipment and other sources of reactor coolant inventory makeup,

except those credited in the safe shutdown analysis depending upon the specific fire area

affected. This safe shutdown strategy was designed to ensure one protected train of equipment

Enclosure 2 transmitted herewith contains SUNSI. When separated from enclosure 2,

this transmittal document is decontrolled.

LIMITED INTERNAL

DISTRIBUTION PERMITTED

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OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

TVA 2

would be available to mitigate a 10 CFR 50, Appendix R related fire in any fire area. A key

feature of this strategy was the LPCI function of RHR to provide long term water inventory

makeup and core cooling. However, the failure of 1-FCV-74-66 rendered the licensees safe

shutdown strategy incapable of accomplishing its safe shutdown functions for those fire areas

that specifically rely on RHR Loop II.

The NRC determined that this finding does not represent an immediate safety concern, because

the Browns Ferry staff has, as part of their immediate corrective actions, implemented repairs

and modifications in accordance with design requirements that returned 1-FCV-74-66 to an

operational condition. Also, the Browns Ferry staff conducted an internal inspection of the RHR

Loop I LPCI outboard injection valve (1-FCV-74-52) while the unit was shutdown. The 1-FCV-

74-52 was determined to be intact with no apparent damage or significant degradation.

Furthermore, as extent of condition compensatory measures, the Browns Ferry staff conducted

and continues to perform a combination of internal inspections, partial motor-operated valve

actuator testing, ultrasonic testing, shutdown cooling operation, and/or monthly venting to verify

proper conditions on the Unit 2 and 3, FCV-74-52 and FCV-74-66 LPCI outboard injection

valves.

The finding is also an apparent violation of Unit 1 Technical Specifications (TS) Limiting

Condition for Operations (LCO) 3.5.1, Emergency Core Cooling System (ECCS) - Operating, in

that between March 13, 2009, and October 23, 2010, the Loop II RHR subsystem was

inoperable for a time in excess of the seven day allowed outage time. This apparent violation is

being considered for escalated enforcement action in accordance with the Enforcement Policy,

which can be found on the NRCs Web site at http://www.nrc.gov/about-

nrc/regulatory/enforcement/enforce-pol.html.

In accordance with NRC Inspection Manual Chapter (IMC) 0609, we intend to complete our

evaluation using the best available information and issue our final determination of safety

significance within 90 days of the date of the enclosed report. The significance determination

process encourages an open dialogue between the NRC staff and the licensee; however, the

dialogue should not impact the timeliness of the staffs final determination.

Before we make a final decision on this matter, we request your attendance at a Regulatory

Conference where you can present to the NRC your perspective on the facts and assumptions

the NRC used to arrive at the finding and assess its significance. The Regulatory Conference

will be open for public observation. We will contact you separately regarding the final

arrangements for the conference. The Regulatory Conference should be held within 30 days of

the receipt of this letter and we encourage you to submit supporting documentation at least one

week prior to the conference in an effort to make the conference more efficient and effective. If

you decline a Regulatory Conference, you relinquish your right to appeal the final SDP

determination, in that by not doing so, you fail to meet the appeal requirements stated in the

Prerequisite and Limitation sections of Attachment 2 of IMC 0609.

Please contact Eugene Guthrie at 404-997-4662 and in writing within 10 days from the issue

date of this letter to notify the NRC of your intentions. If we have not heard from you within 10

days, we will continue with our significance determination and enforcement decision. The final

resolution of this matter will be conveyed in separate correspondence.

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

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TVA 3

Because the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for these inspection findings at this time. In addition, please be advised that the

number and characterization of the apparent violation described in the enclosed inspection

report may change as a result of further NRC review.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and

Enclosure 1 will be made available electronically for public inspection in the NRC Public

Document Room or from the NRCs document system (ADAMS), accessible from the NRC Web

site at http://www.nrc.gov/reading-rm/adams.html. However, because of the security-related

information contained in Enclosure 2, and in accordance with 10 CFR 2.390, a copy of

Enclosure 2 will not be available for public inspection.

Sincerely,

/RA/

Richard P. Croteau, Director

Division of Reactor Projects

Docket No.: 50-259

License No.: DPR-33

Enclosures: 1. NRC Inspection Report 05000259/2010005, 05000260/2010005, and

05000296/2010005

2. SDP Phase 3 Summary (OFFICIAL USE ONLY - SECURITY-

RELATED INFORMATION)

cc w/encl: (See page 4)

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

_________________________ G SUNSI REVIEW COMPLETE

OFFICE RII:DRP RII:DRP RII:DRP RII:EICS RII:DRS OE NRR

SIGNATURE EFG /RA/ WBJ /RA/ RXC /RA/ CFE /RA/ RHB /RA/ Via email Via email

NAME EGuthrie WJones RCroteau CEvans RBernhard CHolt MAshley

DATE 03/01/2011 03/01/2011 03/02/2011 03/01/2011 03/01/2011 02/28/2011 02/28/2011

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

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TVA 4

cc w/encl: James L. McNees, CHP

K. J. Polson Director

Vice President Office of Radiation Control

Browns Ferry Nuclear Plant Alabama Dept. of Public Health

Tennessee Valley Authority P. O. Box 303017

Electronic Mail Distribution Montgomery, AL 36130-3017

C.J. Gannon

General Manager

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

J. E. Emens

Manager, Licensing

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

T. C. Matthews

Manager, Corporate Nuclear Licensing -

BFN

Tennessee Valley Authority

Electronic Mail Distribution

State Health Officer

Alabama Dept. of Public Health

RSA Tower - Administration

Suite 1552

P.O. Box 30317

Montgomery, AL 36130-3017

E. J. Vigluicci

Assistant General Counsel

Tennessee Valley Authority

Electronic Mail Distribution

Chairman

Limestone County Commission

310 West Washington Street

Athens, AL 35611

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OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

TVA 5

Letter to R. M. Krich from Richard P. Croteau dated March 2, 2011

SUBJECT: NRC REPORT 05000259/2010005, 05000260/2010005, AND

05000296/2010005; PRELIMINARY GREATER THAN GREEN FINDING

BROWNS FERRY NUCLEAR PLANT

Distribution w/encl:

RidsNrrPMBrownsFerry Resource

C. Evans, RII

L. Douglas, RII

B. Westreich, NSIR

E. McNiel, NSIR

RIDSNRRDIRS

OE Mail

Public

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

February 9, 2011

EA-11-012

Mr. R. M. Krich

Vice President, Nuclear Licensing

Tennessee Valley Authority

3R Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000259/2010005, 05000260/2010005, 05000296/2010005, AND

NOTICE OF VIOLATION

Dear Mr. Krich:

On December 31, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection

report documents the inspection results which were discussed on January 11, 2011 with Mr.

Keith Polson and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations, orders, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

This report documents one self-revealing apparent violation (AV) concerning the failure of a Unit

1 Residual Heat Removal (RHR) system low pressure injection valve. This violation has

potential safety significance greater than very low safety significance (Green). The violation did

not present an immediate safety concern because Unit 1 was shutdown for a refueling outage

and the other division of RHR was operable and available for service. Additionally, the licensee

repaired the low pressure injection valve prior to the startup of Unit 1. This violation with the

supporting circumstances and details are documented in the inspection report.

Additionally, the NRC has determined that a Severity Level IV violation of NRC requirements

occurred. The violation was evaluated in accordance with the NRC Enforcement Policy. This

violation is cited in the enclosed Notice of Violation (EA-11-012) and the circumstances

surrounding it are described in detail in the subject inspection report. The violation is being

cited in the enclosed Notice because information provided in the second revision of LER

05000296/2009-003 was also not complete and accurate in all material respects. This violation

is being cited because the criterion specified in Section 2.3.2.a.3 of the NRC Enforcement

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Enclosure 1

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

TVA 2

Policy for a non-cited violation was not met. This criterion was not met because the violation

was repetitive and identified by the NRC. The initial violation, also identified by the NRC, was

documented in NRC inspection report 50-296/2010-003. The current Enforcement Policy is

included on the NRC's Web site at http://www.nrc.gov/about-nrc/regulatory/enforcement/

enforce-pol.htmlhttp://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. If you have additional information that you

believe the NRC should consider, you may provide it in your response to the Notice. The NRC

review of your response to the Notice will also determine whether further enforcement action is

necessary to ensure compliance with regulatory requirements.

Furthermore, this report contains one self-revealing finding that was evaluated under the risk

significance determination process as having very low safety significance (Green). The NRC

has also determined that a violation is associated with this finding. This violation is being

treated as a Non-Cited Violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy.

The NCV is described in the subject inspection report. If you contest this violation or

significance of the NCV, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington DC 20555-0001, with copies to: (1) the Regional

Administrator, Region II; (2) the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and (3) the Senior Resident Inspector at

Browns Ferry Nuclear Plant.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response, will be available electronically for public inspection in the NRC

Public Document Room or from the Publicly Available Records (PARS) component of the NRCs

document system (ADAMS),accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html. To the extent possible, your response should not include any personal, privacy

or proprietary information so that it can be made available to the public without redaction.

Sincerely,

/RA/

Eugene F. Guthrie, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-259, 50-260, 50-296

License Nos.: DPR-33, DPR-52, DPR-68

Enclosures:

1. Notice of Violation

2. NRC Integrated Inspection Report 05000259/2010005, 05000260/2010005,

05000296/2010005

cc w/encl. (See page 3)

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Enclosure 1

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

TVA 3

cc w/encl:

K. J. Polson

Vice President

Browns Ferry Nuclear Plant

Tennessee Valley Authority

P.O. Box 2000

Decatur, AL 35609

C. J. Gannon

General Manager

Browns Ferry Nuclear Plant

Tennessee Valley Authority

P.O. Box 2000

Decatur, AL 35609

J. E. Emens

Manager, Licensing and Industry Affairs

Browns Ferry Nuclear Plant

Tennessee Valley Authority

P.O. Box 2000

Decatur, AL 35609

E. J. Vigluicci

Assistant General Counsel

Tennessee Valley Authority

6A West Tower

400 West Summit Hill Drive

Knoxville, TN 37902

State Health Officer

Alabama Dept. of Public Health

RSA Tower - Administration

Suite 1552

P.O. Box 30317

Montgomery, AL 36130-3017

Chairman

Limestone County Commission

310 West Washington Street

Athens, AL 35611

James L. McNees, CHP

Director

Office of Radiation Control

Alabama Dept. of Public Health

P. O. Box 303017

Montgomery, AL 36130-3017

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Enclosure 1

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

TVA 4

Letter to R. M. Krich from Eugene Guthrie dated February 9, 2011

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000259/2010005, 05000260/2010005, 05000296/2010005, AND

NOTICE OF VIOLATION

Distribution w/encl:

C. Evans, RII

L. Douglas, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMBrownsFerry Resource

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

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NOTICE OF VIOLATION

Tennessee Valley Authority Docket No. 50-296

Browns Ferry Nuclear Plant License No. DPR-68

EA-11-012

During an NRC inspection conducted on December 6, 2010, a violation of NRC requirements

was identified. In accordance with the NRC Enforcement Policy, the violation is listed below:

10 CFR 50.9, Completeness and Accuracy of Information, stated in part, that

Information provided to the Commission by a licensee shall be complete and accurate

in all material respects.

Contrary to the above, on August 31, 2010, the licensee submitted a revised LER, as a

corrective action for a previous 10 CFR 50.9 violation involving inoperability of the Unit 3

RCIC system, that was not complete and accurate in all material respects. The revised

LER did not report the correct event date, nor did it describe prior corrective actions

(e.g., maintenance and testing) taken for a previous related event and why these

corrective actions did not prevent recurrence (as specifically detailed in NCV

05000296/2010003-03).

This is a Severity Level IV violation.

Pursuant to the provisions of 10 CFR 2.201, the Tennessee Valley Authority is hereby required

to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional

Administrator, Region II, and a copy to the NRC Senior Resident Inspector at the facility that is

the subject of this Notice, within 30 days of the date of the letter transmitting this Notice of

Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of Violation; EA-

11-012" and should include for each violation: (1) the reason for the violation, or, if contested,

the basis for disputing the violation or severity level, (2) the corrective steps that have been

taken and the results achieved, (3) the corrective steps that will be taken, and (4) the date when

full compliance will be achieved. Your response may reference or include previous docketed

correspondence, if the correspondence adequately addresses the required response. If an

adequate reply is not received within the time specified in this Notice, an order or a Demand for

Information may be issued as to why the license should not be modified, suspended, or

revoked, or why such other action as may be proper should not be taken. Where good cause is

shown, consideration will be given to extending the response time. If you contest this

enforcement action, you should also provide a copy of your response, with the basis for your

denial, to the Director, Office of Enforcement, United States Nuclear Regulatory Commission,

Washington, DC 20555-0001.Because your response will be made available electronically for

public inspection in the NRC Public Document Room or from the NRCs document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to

the extent possible, it should not include any personal privacy, proprietary, or safeguards

information so that it can be made available to the public without redaction. If personal privacy

or proprietary information is necessary to provide an acceptable response, then please provide

a bracketed copy of your response that identifies the information that should be protected and a

redacted copy of your response that deletes such information. If you request withholding of

such material, you must specifically identify the portions of your response that you seek to have

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Enclosure 1

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2

withheld and provide in detail the bases for your claim of withholding (e.g., explain why the

disclosure of information will create an unwarranted invasion of personal privacy or provide the

information required by 10 CFR 2.390(b) to support a request for withholding confidential

commercial or financial information). If safeguards information is necessary to provide an

acceptable response, please provide the level of protection described in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 9th day of February 2011.

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Enclosure 1

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-259, 50-260, 50-296

License Nos.: DPR-33, DPR-52, DPR-68

Report No.: 05000259/2010005, 05000260/2010005, 05000296/2010005

Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3

Location: Corner of Shaw and Nuclear Plant Roads

Athens, AL 35611

Dates: October 1, 2010 through December 31, 2010

Inspectors: T. Ross, Senior Resident Inspector

C. Stancil, Resident Inspector

P. Niebaum, Resident Inspector

L. Pressley, Resident Inspector

A. Rogers, Reactor Inspector (1R08)

R. Baldwin, Senior Operations Engineer (1R11.2)

E. Lea, Senior Operations Engineer (1R11.3)

G. Johnson, Operations Engineer (1R11.3)

C. Kontz, Senior Project Engineer (4OA2.4, 4OA5.4)

M. King, Senior Project Inspector (4OA2.4)

J. Wray, Senior Enforcement Specialist (4OA5.4)

L. Jarriel, Agency Allegation Advisor (4OA5.4)

Approved by: Eugene F. Guthrie, Chief

Reactor Projects Branch 6

Division of Reactor Projects

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Enclosure 1

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SUMMARY OF FINDINGS

IR 05000259/2010005, 05000260/2010005, 05000296/2010005; 10/01/2010 - 12/31/2010;

Browns Ferry Nuclear Plant, Units 1, 2 and 3; Refueling and Other Outage Activities, Event

Follow-up.

The report covered a three month period of inspection by the resident inspectors, two senior

reactor operations engineers, a reactor operations engineer, two senior project engineers and a

reactor inspector from Region II. One apparent violation (AV), one severity level IV cited

violation (VIO), and one non-cited violation (NCV) were identified. The significance of most

findings is identified by their color (Green, White, Yellow, Red) using Inspection Manual Chapter

(IMC) 0609, Significance Determination Process (SDP); the cross-cutting aspect was

determined using IMC 0310, Components Within the Cross-Cutting Areas. Findings for which

the SDP does not apply may be Green or be assigned a severity level after NRC management

review. The NRCs program for overseeing the safe operation of commercial nuclear power

reactors is described in NUREG-1649, Reactor Oversight Process Revision 4, dated

December 2006.

A. NRC Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

(TBD). A self-revealing Apparent Violation (AV) of Unit 1 Technical Specifications

(TS) Limiting Condition for Operations (LCO) 3.5.1, Emergency Core Cooling System

(ECCS) - Operating, was identified for the licensees failure to comply with the TS

LCO required actions for an inoperable Residual Heat Removal (RHR) and Low

Pressure Coolant Injection (LPCI) subsystem due to a failure of the RHR Loop II

LPCI Outboard Injection Valve (1-FCV-74-66) to open. The licensee entered this

issue into their corrective action program as problem evaluation report (PER)

271338. The 1-FCV-74-66 was subsequently repaired and returned to service

during the Unit 1 outage prior to restart.

This finding has potential safety significance greater than very low safety significance

(Green) and will remain indeterminate pending completion of the significance

determination process. The inspectors determined that the licensees failure to

establish adequate design control and perform adequate maintenance on the Unit1

outboard LPCI injection valve, 1-FCV-74-66, which resulted in the valve being left in

a significantly degraded condition and RHR loop II unable to fulfill its safety function,

was a performance deficiency. This finding was considered more than minor

because it was associated with the Protection Against External Factors attribute of

the Reactor Safety/ Mitigating Systems Cornerstone and adversely affected the

cornerstone objective of ensuring availability and reliability of systems designed to

respond to initiating events to prevent undesirable consequences. Specifically, the

RHR subsystem was rendered incapable of being aligned to perform its safe

shutdown function due to the failure of 1-FCV-74-66. The safety characterization of

this finding is not yet finalized and is currently characterized as To Be Determined

(TBD). This finding does not have a cross-cutting aspect because it is not reflective

of current licensee performance in the last three years. (Section 1R20.1(1))

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Enclosure 1

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3

  • Green. A self-revealing non-cited violation (NCV) of Unit 1 Technical Specifications

(TS) Limiting Condition for Operations (LCO) 3.6.2.3, Suppression Pool Cooling was

identified for the licensees failure to correct a degraded condition of the 1C Residual

Heat Removal (RHR) pump motor that rendered it inoperable for greater than the TS

allowed outage time of 30 days. Specifically, the 1C RHR pump motor suffered a

catastrophic failure on October 27, 2010 and was subsequently determined to have

been in a degraded condition since November 2007. This condition would have

prevented the pump from performing its intended safety functions during the

systems required mission time. The licensee entered this issue into the corrective

action program as problem evaluation report (PER) 274840. The 1C RHR pump

motor was subsequently repaired during the Unit 1 refueling outage and returned to

service on November 10, 2010 prior to Unit 1 restart.

This performance deficiency was considered greater than minor because it was

associated with the Mitigating Systems cornerstone and adversely affected the

equipment performance objective to ensure the availability and capability of the RHR

system to respond to initiating events to prevent undesirable consequences (i.e.,

core damage). Specifically, the 1C RHR subsystem was degraded to the point that it

was incapable of performing its intended safety functions for the systems required

mission time. Since the 1C RHR pump motor failure occurred during Mode 5

shutdown conditions after a significant period of shutdown cooling operation, the

finding was evaluated according to Inspection Manual Chapter 609, Appendix G,

Shutdown Operations Significance Determination Process, Attachment 1, Phase 1

Operational Checklists, Checklist 7, Refueling Operation with Reactor Coolant Level

Above 23. Accordingly, the finding was determined to be of very low safety

significance (Green) because the 1A RHR pump and the Auxiliary Decay Heat

Removal (ADHR) system were available, when only one RHR pump was needed per

Section I.C of Checklist 7. The cause of this finding was directly related to the cross

cutting aspect of Thorough Evaluation of Identified Problems in the Corrective Action

Program component of the Problem Identification and Resolution area, because the

licensee did not adequately evaluate the precursors related to the degraded 1C RHR

motor performance and properly prioritize the resolution of a known condition

adverse to quality in time to preclude motor failure P.1(c). (Section 1R20.1(2))

B. Licensee Identified Violations

None.

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Enclosure 1

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REPORT DETAILS

Summary of Plant Status

Unit 1 operated at full Rated Thermal Power (RTP) for most of the report period except for three

unplanned downpowers, and a scheduled refueling outage (RFO). On October 4, 2010, an

unplanned downpower to approximately 94 percent RTP occurred due to a power cell failure in

the 1B variable frequency drive (VFD). Unit 1 returned to full RTP later that same day. On

October 23, 2010, Unit 1 was shutdown for a scheduled refueling outage that lasted 31 days.

The unit was restarted on November 22, 2010. During the power ascension, there was a

planned downpower from approximately 60% to 30% RTP on November 24, 2010, for single

loop operations in order to repair a power cell in the 1A VFD. The unit returned to full RTP on

November 25, 2010. On December 2, 2010, Unit 1 experienced an unplanned downpower to

45 percent RTP due to failures of a 1A VFD power cell. The unit returned to full RTP on

December 3, 2010 following repairs to the 1A VFD unit.

Unit 2 operated at essentially full RTP the entire report period except for two planned

downpowers. On October 24, 2010, a planned downpower to 90 percent RTP was conducted

to support a control rod exercise and the unit returned to full RTP later that same day. On

December 11, 2010, a planned downpower to 70 percent RTP was conducted to support a

control rod sequence exchange and the unit returned to full RTP later that same day.

Unit 3 operated at essentially full RTP the entire report period except for three planned

downpowers and one unplanned reactor shutdown. On October 3, 2010, a planned downpower

to 94 percent RTP was conducted for a control rod exercise and the unit returned to full RTP

later that same day. On October 26, 2010 a planned downpower to 93 percent RTP was

conducted for a control rod exercise and the unit returned to full RTP later that same day. On

December 17, 2010 a planned downpower was conducted to support a control rod sequence

exchange and the unit returned to full RTP later that same day. On December 26, 2010, Unit 3

experienced an unplanned downpower to 90 percent RTP followed by a manual reactor scram

due to high vibration on the main generator exciter bearings. Unit 3 remained shutdown through

the end of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

.1 Impending Adverse Weather Conditions - Cold Weather

a. Inspection Scope

On December 13th, 14th and 15th an adverse cold weather advisory was issued for the

Northern Alabama area. The inspectors reviewed the licensee=s overall

preparations/protection for the expected weather conditions and observed the licensees

implementation of general operating instruction GOI-200-1, Freeze Protection

Inspection. The inspectors also reviewed and discussed the implementation of

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GOI-200-1 with the responsible Unit Supervisors and Shift Managers. Furthermore, the

inspectors witnessed the licensees execution of freeze protection of vulnerable areas

and buildings inside and outside the power block. The inspectors also verified operator

staffing for the given conditions was adequate and reviewed any active, upcoming and

delayed work orders and surveillances. The inspectors also verified completion of the

freeze protection checklists. This satisfied one inspection sample.

b. Findings

No findings were identified.

.2 Impending Adverse Weather Conditions - Tornado Warning

a. Inspection Scope

On October 26, 2010, a Tornado Warning was declared for adjacent counties. The

inspectors reviewed the licensee=s overall preparations/protection for the expected

weather conditions and observed the licensees implementation of abnormal operating

instruction (AOI) 100-7, Severe Weather. The inspectors also reviewed and discussed

the implementation of AOI 100-7 with the responsible Unit Supervisor and Shift

Manager; along SSI-19.1, Post Requirements and Responsibilities, Temporary

Suspension of Security Measures, Tornado Emergency Guide/Checkoff with Security

supervision. Furthermore, the inspectors witnessed the licensees execution of

evacuation orders of vulnerable areas and buildings in and outside the power block,

including the termination of work and evacuation of the main turbine deck and refueling

floor. The inspectors also conducted walkdowns of critical plant areas and a general tour

of the plant grounds. Lastly, the inspectors reviewed available operator and security

staffing, and verified access controls and indications for those systems required for safe

control and physical protection of the plant. This satisfied one inspection sample.

b. Findings

No findings were identified.

.3 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors reviewed licensee procedure 0-GOI-200-1, Freeze Protection Inspection,

and reviewed licensee actions to implement the procedure in preparation for cold

weather conditions. The inspectors also reviewed the list of open Problem Evaluation

Reports (PERs) to verify that the licensee was identifying and correcting potential

problems relating to cold weather operations. In addition, the inspectors reviewed

procedure requirements and walked down selected areas of the plant, which included

residual heat removal service water (RHRSW) system and Emergency Equipment

Cooling Water (EECW) system rooms, Emergency Diesel Generators (EDGs) building,

and systems in the Intake Structure, to verify that affected systems and components

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were properly configured and protected as specified by the procedure. Furthermore, the

inspectors discussed cold weather conditions with Operations personnel to assess plant

equipment conditions and personnel sensitivity to upcoming cold weather conditions.

During actual cold weather conditions the later part of December, when outside

temperatures dropped below the 32 degree Fahrenheit (F) and 25F thresholds of 0-GOI-

200-1, the inspectors conducted walkdown tours of the main control rooms to assess

system performance and alarm conditions of systems susceptible to cold weather

conditions. In addition, the inspectors verified effectiveness of licensee implementation

of procedure EPI-0-000-FRZ001, Freeze Protection Program for RHRSW Pump Rooms,

to ensure RHRSW system and components were not adversely affected by the cold

weather. Furthermore, the inspectors verified that the applicable equipment walkdown

checklists required by 0-GOI-200-1 were implemented accordingly. This satisfied one

inspection sample.

b. Findings

No findings were identified.

.4 Readiness to Cope with External Flooding

a. Inspection Scope

The inspectors reviewed plant design features and licensee procedures intended to

protect the plant and its safety-related equipment from external flooding events. The

inspectors reviewed licensing basis flood analysis documents including: Updated Final

Safety Analysis Report (UFSAR) Section 2.4, Hydrology, Water Quality, and Marine

Biology, which included Appendix 2.4A, Maximum Possible Flood; UFSAR Section

12.2.9.2.3 Flood Gate, and BFN-50-C-7101, Protection from Wind, Tornado Wind,

Tornado Depressurization, Tornado Generated Missiles, and External Flooding. The

inspectors performed walkdowns of risk-significant areas, susceptible systems and

equipment, including the common Unit 1/2 A, B, C and D emergency diesel

generator (EDG) rooms and the Unit 3 EDG rooms 3A,3B, 3C, and 3D. The

inspectors review included flood-significant features such as the portable bulkhead used

as a temporary flood barrier, sump pump flowrates, sump drains and level switch

setpoints and watertight door seals for the common U1/2 EDG building and the U3

diesel generator building. Plant procedures and calculations for coping with flooding

events were also reviewed to verify that licensee actions and maintenance practices

were consistent with the plants design basis assumptions.

The inspectors also reviewed licensee corrective action documents for flood-related

items identified in PERs written from 2009 through early 2010 to verify the adequacy of

the corrective actions. The inspectors reviewed selected completed preventive

maintenance procedures and work orders for identified level switches, pumps and flood

barriers (e.g., Flood Doors) for completeness and frequency. This satisfied one

inspection sample.

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b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns to evaluate the

operability of selected redundant trains or backup systems, listed below, while the other

train or subsystem was inoperable or out of service. The inspectors reviewed the

functional systems descriptions, UFSAR, system operating procedures, and Technical

Specifications (TS) to determine correct system lineups for the current plant conditions.

The inspectors performed walkdowns of the systems to verify that critical components

were properly aligned and to identify any discrepancies which could affect operability of

the redundant train or backup system. Documents reviewed are listed in the

Attachment.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Fire Protection Tours

a. Inspection Scope

The inspectors reviewed licensee procedures, Standard Programs and Processes

(SPP)-10.10, Control of Transient Combustibles, and SPP-10.9, Control of Fire

Protection Impairments, and conducted a walkdown of the four fire areas (FA) and fire

zones (FZ) listed below. Selected FAs/FZs were examined in order to verify licensee

control of transient combustibles and ignition sources; the material condition of fire

protection equipment and fire barriers; and operational lineup and operational condition

of fire protection features or measures. Also, the inspectors verified that selected fire

protection impairments were identified and controlled in accordance with procedure

SPP-10.9. Furthermore, the inspectors reviewed applicable portions of the Site Fire

Hazards Analysis Volumes 1 and 2 and Pre-Fire Plan drawings to verify that the

necessary firefighting equipment, such as fire extinguishers, hose stations, ladders, and

communications equipment, was in place.

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  • Unit 3 Fire Zone 3-2 EL 519 through 565, from column line R21 to 10 ft west of

column line R18.

  • Unit 3 4kV Shutdown Board 3EA,3EB (FA - 22)
  • Unit 3 4kV Shutdown Board 3EC, 3ED (FA - 23)
  • Unit 3 4kV Bus Tie Board (FA - 24)

b. Findings

No findings were identified.

1R08 Inservice Inspection (ISI) Activities (IP 71111.08B, Unit 1)

a. Inspection Scope

From November 1 through November 5, 2010, the inspectors observed and reviewed

the implementation of the licensee=s In-service Inspection (ISI) program for monitoring

degradation of the reactor coolant system (RCS) boundary and risk-significant piping

boundaries of Browns Ferry Unit 1 during the autumn 2010 refueling outage. The

inspectors= activities consisted of an on-site review of nondestructive examination (NDE)

and welding activities to evaluate compliance with Technical Specifications and the

applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and

Pressure Vessel Code, Sections XI and V (Code of record: 2001 Edition through the

2003 Addenda), for Class 1, 2, and 3 systems; and to verify that indications and defects

(if present) were appropriately evaluated and dispositioned in accordance with the

requirements of the ASME Code Section XI acceptance standards. For Browns Ferry

Unit 1, this was second outage in the first period of the second 10-year ISI inspection

interval. The inspectors also reviewed a sample of inspection activities associated with

components that were outside the scope of ASME Section XI requirements which were

performed in accordance with commitments to follow industry guidance documents, such

as the Boiling Water Reactor Vessel and Internals Project (BWRVIP).

.1 Piping Systems ISI.

a. Inspection Scope

The inspectors reviewed NDE activities, both by direct observation and record review,

specifically including examination procedures, NDE reports, equipment and

consumables certification records, personnel qualification records, and calibration

reports for compliance to requirements of ASME Section V, ASME Section XI, BWRVIP

documents, and other industry standards for the following examinations:

  • Penetrant Testing (PT)

o Feedwater Weld Overlay, Weld #: RFW-1-028-001

o RHR Weld Attachment to Pipe, Weld #: 1-47B452-3047-IA

o Recirculation Weld Attachment to Pipe, Weld #: 1-47B465-462-IA

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  • Ultrasonic Testing (UT)

o Feedwater Weld Overlay, Weld #: RFW-1-028-001

o Feedwater Pipe, Weld #: GFW-1-08

o Feedwater Pipe Butt Weld, Weld #: N-11B-1

o Feedwater Pipe Weld Overlay, Weld #: N-11B-1-OL

o Feedwater Pipe Weld Overlay, Weld #: RFW-1-028-001

o Feedwater Pipe, Weld #: KFW-1-29

o Feedwater Pipe, Weld #: KFW-1-38

o Feedwater Pipe, Weld #: KFW-1-39

o Recirculation System, Weld #: RWR-1-002-042

The inspectors conducted a Unit 1 containment walk-down of multiple drywell elevations

to assess, in general, the material condition of structures, systems, and components,

including leaks from bolted connections, coating integrity, cleanliness, hangers and

supports, etc.

The inspectors also reviewed welding activities from last outage for the following Class 1

and 2 components:

  • Base Metal repairs to the cladding on the Reactor Vessel Head Flange

The inspectors completed a review of ISI-related problems that were identified by the

licensee and entered into the corrective action program. The inspectors reviewed these

corrective action documents to confirm that the licensee had appropriately described the

scope of the problems, and had implemented appropriate corrective actions. The

inspectors= review included confirmation that the licensee had an adequate threshold for

identifying issues. Through interviews with licensee staff and review of corrective action

documents, the inspectors evaluated the licensee=s threshold for identifying lessons

learned from industry issues related to ASME Section XI. The inspectors performed

these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI,

ACorrective Action,@ requirements. The corrective action documents reviewed by the

inspectors are listed in the Attachment.

b. Findings

No findings were identified.

.2 Reactor Vessel Internal Inspections

a. Inspection Scope

The inspectors reviewed the following NDE activities associated with the inspection of

Reactor Vessel internal components (Boiling Water Reactors Vessel Internals Project):

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  • Visual Testing (VT)

o Jet Pump assemblies on shroud and vessel side

o Core Spray P4A downcomer

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On October 19, 2010, the inspectors observed two licensed operator requalification

(LOR) program annual simulator examinations for an Operations group. During each

exam the senior reactor operator and the reactor operator positions were rotated, except

for the shift manager. The examinations observed by the inspectors were the 2010 LOR

Exam-02 and the LOR Exam-13.

The inspectors specifically evaluated the following attributes related to each operating

crews performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of Abnormal Operating Instructions (AOIs), and

Emergency Operating Instructions (EOIs)

  • Timely and appropriate Emergency Action Level declarations per Emergency Plan

Implementing Procedures (EPIP)

  • Control board operation and manipulation, including high-risk operator actions
  • Command and Control provided by the US and Shift Manager (SM)

The inspectors attended a post-examination critique to assess the effectiveness of the

licensee evaluators, and to verify that licensee-identified issues were comparable to

issues identified by the inspector. The inspectors also reviewed simulator physical

fidelity (i.e., the degree of similarity between the simulator and the reference plant

control room, such as physical location of panels, equipment, instruments, controls,

labels, and related form and function).

b. Findings

No findings were identified.

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.2 Annual Review of Licensee Requalification Examination Results

a. Inspection Scope

October 20, 2010, the licensee completed the comprehensive biennial requalification

written examinations and annual requalification operating tests required to be

administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The

inspectors performed an in-office review of the overall pass/fail results of the written

examinations, individual operating tests and the crew simulator operating tests. These

results were compared to the thresholds established in Inspection Manual Chapter 609,

Appendix I, Operator Requalification Human Performance Significance Determination

Process.

b. Findings

No findings were identified.

.3 Biennial Review

a. Inspection Scope

The inspectors reviewed the facility operating history and associated documents in

preparation for this inspection. During the week of October 12, 2010, the inspectors

reviewed documentation, interviewed licensee personnel, and observed the

administration of operating tests associated with the licensees operator requalification

program. Each of the activities performed by the inspectors was done to assess the

effectiveness of the facility licensee in implementing requalification requirements

identified in 10 CFR Part 55, Operators Licenses. The evaluations were also

performed to determine if the licensee effectively implemented operator requalification

guidelines established in NUREG-1021, Operator Licensing Examination Standards for

Power Reactors, and Inspection Procedure 71111.11, Licensed Operator

Requalification Program. The inspectors also evaluated the licensees simulation

facility for adequacy for use in operator licensing examinations using ANSI/ANS-3.5-

1981, American National Standard for Nuclear Power Plant Simulators for use in

Operator Training and Examination. The inspectors observed three crews during the

performance of the operating tests. Documentation reviewed included written

examinations, Job Performance Measures (JPMs), simulator scenarios, licensee

procedures, on-shift records, simulator modification request records, simulator

performance test records, operator feedback records, licensed operator qualification

records, remediation plans, watchstanding records, and medical records. These records

were inspected using the criteria listed in Inspection Procedure 71111.11. Documents

reviewed during the inspection are documented in the List of Documents Reviewed.

b. Findings

No findings were identified.

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1R12 Maintenance Effectiveness

.1 Routine

a. Inspection Scope

The inspectors examined two specific equipment issues listed below for structures,

systems and components (SSC) within the scope of the Maintenance Rule (MR)

(10CFR50.65) with regard to some or all of the following attributes, as applicable:

(1) Appropriate work practices; (2) Identifying and addressing common cause failures;

(3) Scoping in accordance with 10 CFR 50.65(b) of the MR; (4) Characterizing reliability

issues for performance monitoring; (5) Charging unavailability for performance

monitoring; (6) Balancing reliability and unavailability; (7) Trending key parameters for

condition monitoring; (8) System classification and reclassification in accordance with 10

CFR 50.65(a)(1) or (a)(2); (9) Appropriateness of performance criteria in accordance

with 10 CFR 50.65(a)(2); and (10) Appropriateness and adequacy of (a)(1) goals and

corrective actions (i.e.- Ten Point Plan). The inspectors also compared the licensees

performance against site procedure SPP-6.6, Maintenance Rule Performance Indicator

Monitoring, Trending and Reporting; Technical Instruction 0-TI-346, Maintenance Rule

Performance Indicator Monitoring, Trending and Reporting; and SPP 3.1, Corrective

Action Program. The inspectors also reviewed, as applicable, work orders, surveillance

records, PERs, system health reports, engineering evaluations, and MR expert panel

minutes; and attended MR expert panel meetings to verify that regulatory and procedural

requirements were met.

  • Units 1, 2, and 3 CS Systems Excessive Unavailability
  • Failure of Magnesium Rotors in Safety-Related Motor Actuated Valve Actuators

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For planned online work and/or emergent work that affected the combinations of risk

significant systems listed below, the inspectors reviewed three maintenance risk

assessments, and actions taken to plan and/or control work activities to effectively

manage and minimize risk. The inspectors verified that risk assessments and applicable

risk management actions (RMA) were conducted as required by 10 CFR 50.65(a)(4) and

applicable plant procedures such as SPP-7.0, Work Management; NPG-SPP-7.1, On-

Line Work Management; 0-TI-367, BFN Equipment to Plant Risk Matrix; NPG-SPP-7.3,

Work Activity Risk Management Process; and NPG-SPP-7.2, Outage Management.

Furthermore, as applicable, the inspectors verified the adequacy of the licensees risk

assessments, implementation of RMAs, and plant configuration.

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  • On October 13, B Standby Gas Treatment (SBGT) Fan and G Control Air

Compressor were out of service (OOS) for maintenance with emergent work on 3C

EDG and B1 RHRSW Pump

  • Unplanned Entry into Unit 1 ORAM Orange Condition Due To ADHR B Primary Heat

Exchanger Leak While Both Divisions of Residual Heat Removal (RHR) OOS

  • Unplanned Entry into Unit 1 ORAM Orange Condition Due To Onset of Severe

Weather While Spent Fuel Gates Installed, and ADHR and Division II RHR OOS

b. Findings

No findings were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the six operability/functional evaluations listed below to verify

technical adequacy and ensure that the licensee had adequately assessed TS

operability. The inspectors also reviewed applicable sections of the UFSAR to verify that

the system or component remained available to perform its intended function. In

addition, where appropriate, the inspectors reviewed licensee procedure NEDP-22,

Functional Evaluations, to ensure that the licensees evaluation met procedure

requirements. Furthermore, where applicable, inspectors examined the implementation

of compensatory measures to verify that they achieved the intended purpose and that

the measures were adequately controlled. The inspectors also reviewed PERs on a

daily basis to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations.

  • Unit 3: 3B EDG Immersion Heater and Circulating Oil Soak Back Pump Standby

Auxiliaries De-Energized in Manual Control (PER 260536)

  • Unit 1 and 2 B EDG Unable to Achieve Maximum Rated Load per UFSAR (PER

209288)

  • C3 EECW Pump Severe Shaft Degradation (PER 257317)

268624)

  • Capability to Parallel Two EDGs on a 4KV Shutdown Board per Design Basis (PER

178142)

  • Holtec MPC-68 Heat Load Limits (PER 255823)

b. Findings

No findings were identified.

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1R18 Plant Modifications

Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the temporary modification listed below and licensee procedure

NPG-SPP-9.5, Temporary Alterations, to verify regulatory requirements were met. The

inspectors also reviewed the associated 10 CFR 50.59 screening and evaluation and

compared each against the UFSAR and TS to verify that the modification did not affect

operability or availability of the affected system. Furthermore, the inspectors walked

down the modification to ensure that it was installed in accordance with the modification

documents and reviewed post-installation and removal testing to verify that the actual

impact on permanent systems was adequately verified by the tests.

Pressurization of Primary Containment

b. Findings

No findings were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the six post-maintenance tests (PMT) listed below to verify that

procedures and test activities confirmed SSC operability and functional capability

following maintenance. The inspectors reviewed the licensees completed test

procedures to ensure any of the SSC safety function(s) that may have been affected

were adequately tested, that the acceptance criteria were consistent with information in

the applicable licensing basis and/or design basis documents, and that the procedure

had been properly reviewed and approved. The inspectors also witnessed the test

and/or reviewed the test data, to verify that test results adequately demonstrated

restoration of the affected safety function(s). The inspectors verified that PMT activities

were conducted in accordance with applicable WO instructions, or procedural

requirements, including NPG-SPP-6.3, Pre-/Post-Maintenance Testing, and MMDP-1,

Maintenance Management System. Furthermore, the inspectors reviewed problems

associated with PMTs that were identified and entered into the CAP.

  • Unit 1: PMT for Installation of Alternate Supply Backup Diesel Generator for ADHR.
  • Unit Common: PMT for Standby Gas Treatment Train B Roughing Filter

Replacement and Outlet Damper Repair Per 0-SR-3.6.4.3.2(B VFTP), Standby Gas

Treatment Filter Pressure Drop and In-Place Leak Tests - Train B

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Loop Valve Stem/Disc Separation Repair Per Work Orders (WOs) 111571105,

111571764, and 09-723979-000; and 1-SR-3.6.1.3.5(RHR II), RHR System MOV

Operability Loop II; and 1-SR-3.3.3.1.4(H II), Verification of Remote Position

Indicators for RHR System II Valves.

Per WOs 09-723912-000 and 09-723911-000; ECI-0-000-RLY003, Replacement of

Relays; EPI-0-099-RLY001, Reactor Protection System Scram Solenoid and Reset

Relays Channel A; and EPI-0-099-RLY002, Reactor Protection System Scram

Solenoid and Reset Relays Channel B

and 2-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow

Rate Test at Rated Reactor Pressure

  • Unit 3: PMT for Core Spray Division II Preventive Maintenance per 3-SR-

3.5.1.6(CSII), Core Spray Flow Rate Loop II, and applicable WOs

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

.1 Unit 1 Scheduled Refueling Outage (U1R8)

a. Inspection Scope

From October 23 through November 23, 2010, the inspectors examined critical outage

activities associated with the U1R8 refueling outage and the Unit 1 restart to verify that

they were conducted in accordance with TS, applicable operating procedures, and the

licensees outage risk assessment and management plans. Some of the more

significant inspection activities conducted by the inspectors were as follows:

Outage Risk Assessment

Prior to the Unit 1 scheduled U1R8 refueling outage that began on October 23, the

inspectors met with outage risk assessment team members and reviewed the Outage

Risk Assessment Report to verify that the licensee had appropriately considered risk,

industry experience, and previous site-specific problems in developing and implementing

an outage plan that assured the necessary levels of defense-in-depth of safety functions

were maintained. The inspectors also reviewed the daily U1R8 Refueling Outage

Reports, including the Outage Risk Assessment Management (ORAM) Safety Function

Status, and regularly attended the licensees outage status meetings. These reviews

were compared to the requirements in licensee procedure NPG-SPP-07.2, Outage

Management. These reviews were also done to verify that for identified high risk

significant conditions, due to equipment availability, severe weather and/or system

configurations, that contingency measures were identified and incorporated into the

overall outage and contingency response plan. Furthermore, the inspectors frequently

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discussed risk conditions and designated protected equipment with Operations and

outage management personnel to assess licensee awareness of actual risk conditions

and mitigation strategies.

Shutdown and Cooldown Process

The inspectors witnessed the shutdown and cooldown of Unit 1 in accordance with

licensee procedures OPDP-1, Conduct of Operations; 1-GOI-100-12A, Unit Shutdown

from Power Operations to Cold Shutdown and Reduction in Power During Power

Operations; and 1-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring.

Decay Heat Removal

The inspectors reviewed licensee procedures 1-OI-74, Residual Heat Removal System

(RHR); 1-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating

Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted

main control room panel and in-plant walkdowns of system and components to verify

correct system alignment. During planned evolutions that resulted in an increased

outage risk condition of Orange for shutdown cooling, inspectors verified that the plant

conditions and systems identified in the risk mitigation strategy were available. In

addition, the inspectors reviewed controls implemented to ensure that outage work was

not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown

cooling, and/or the ADHR system. Furthermore, the inspectors conducted several

walkdowns of the ADHR system during operation with the fuel pool gates removed.

Critical Outage Activities

The inspectors examined outage activities to verify that they were conducted in

accordance with TS, licensee procedures, and the licensees outage risk control plan.

Some of the more significant inspection activities accomplished by the inspectors were

as follows:

  • Walked down the following selected safety-related equipment clearance orders (i.e.,

tag-outs)

o Tagout 1-TO-2010-0003, Clearance 1-074-0037A, RHR System II

o Tagout 1-TO-2010-0003, Clearance 1-071-0011D, RCIC Bearing Repair

o Tagout 1-TO-2010-0003, Clearance 1-063-0001A, SLC Injection Valve B

  • Verified electrical systems availability and alignment
  • Monitored important main control room plant parameters (e.g., RCS pressure, level,

flow, and temperature) and TS compliance during the various shutdown modes of

operation, and mode transitions

  • Evaluated implementation of reactivity controls
  • Reviewed control of containment integrity

the reactor cavity, equipment pit, and spent fuel pool

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  • Performed routine tours of the control room, reactor building, refueling floor and drywell

Reactor Vessel Disassembly and Refueling Activities

The inspectors witnessed selected activities associated with reactor vessel disassembly,

and reactor cavity flood-up and drain down in accordance with 1-GOI-100-3A, Refueling

Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions,

the inspectors witnessed fuel handling operations during the Unit 1 reactor core fuel

shuffle performed in accordance with TS and applicable operating procedures, such as

GOI-100-3A, Refueling Operations (In Vessel), GOI-100-3B, Operations in the Spent

Fuel Pool, and GOI-100-3C, Fuel Movement Operations During Refueling. The

inspectors verified specific fuel movements as delineated by the Fuel Assembly Transfer

Sheets (FATF).

Drywell Closeout

Between November 19 and November 21, 2010, the inspectors reviewed the licensees

conduct of 1-GOI-200-2, Drywell Closeout, and performed an independent detailed

closeout inspection of the Unit 1 Torus and drywell.

Restart Activities

The inspectors specifically conducted the following:

with 1-SI-3.3.1.A, ASME Section XI System Leakage Test of the Reactor pressure

Vessel and Associated Piping

  • Reviewed and verified completion of selected items of 0-TI-270, Refueling Test

Program, Attachment 2, Startup Review Checklist

Revision 6

  • Attended multiple Unit 1 Restart PORC Meetings
  • Witnessed Unit 1 approach to criticality and power ascension per 1-GOI-100-1A, Unit

Startup, and 1-GOI-100-12, Power Maneuvering

  • Reactor Coolant Heatup/Pressurization to Rated Temperature and Pressure per 1-

SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring

Corrective Action Program

The inspectors reviewed PERs generated during U1R8 and attended management

review committee meetings to verify that initiation thresholds, priorities, mode holds,

operability concerns and significance levels were adequately addressed. Resolution and

implementation of corrective actions of several PERs were also reviewed for

completeness.

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b. Findings

Two findings were identified.

(1) Introduction: A self-revealing apparent violation (AV) of Unit 1 TS Limiting Condition for

Operation (LCO) 3.5.1, Emergency Core Cooling System (ECCS) - Operating, was

identified for the licensees failure to establish adequate design control and perform

adequate maintenance on the Unit 1 outboard Low Pressure Coolant Injection (LPCI)

valve, 1-FCV-74-66, which resulted in the valve being left in a significantly degraded

condition and RHR loop II unable to fulfill its safety function.

Description: On October 23, 2010, RHR Loop II LPCI Outboard Injection Valve, 1-FCV-

74-66 (Walworth 5509, 24 inch 600 pound angle globe valve), failed to open when

operators attempted to place RHR Shutdown Cooling, Loop II, in service to support

U1R8 refueling activities. Control room indications indicated the valve was open but no

flow was indicated in RHR Loop II with the 1B RHR pump in service. Operators

concluded the RHR Loop II flow path was inoperable, and proceeded to secure the 1B

RHR pump and promptly placed RHR Loop I in-service for shutdown cooling. Unit 1 was

in Mode 3 at the time.

Subsequent visual inspections of the FCV-74-66 valve stem, upper disc skirt, disc, skirt

to disc tack welds, and thread engagements identified the following:

  • The valve disc was found to be seated and stuck in the valve seat, essentially

blocking all RHR Loop II flow.

  • The disc was found separated from the stem and upper disc skirt, which would

normally be threaded onto the disc skirt and tack welded.

  • The two 8 inch fillet welds between the disc skirt and the disc were fractured (welds

completely broken apart). Also, further examination discovered the welds to be

undersized.

  • No upper disc skirt locking key was present.
  • The threads on the upper disc skirt were found to be undersized, resulting in partial

engagement of thread faces between the disc skirt and disc.

  • The thrust washer between the stem and disc was missing.

The licensee initiated PER 271338 to determine the root cause of the valve failure. The

licensees root cause analysis of 1-FCV-74-66 was not complete by the end of the

inspection. As part of their immediate corrective actions, the licensee implemented

appropriate repairs and modifications to restore FCV-74-66 prior to Unit 1 restart. Also,

the licensee conducted an internal inspection of the RHR Loop I LPCI outboard injection

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valve (1-FCV-74-52) prior to Unit 1 restart. The FCV-74-52 was determined to be intact

with no apparent damage or significant degradation. Furthermore, as extent of condition

compensatory measures, the licensee has conducted and continued to perform a

combination of internal inspections, partial motor-operated valve actuator testing, UT

testing, shutdown cooling operation, and/or monthly venting to verify proper conditions of

the Unit 2 and 3 FCV-74-52 and 66 LPCI outboard injection valves.

The inspectors found that 1-FCV-74-66 had been modified in 1983 by engineering

change notice ECN L2107 to install a V-notch lower disc skirt which was intended to

eliminate excessive vibrations experienced at low flow and high pressure drop conditions

and provide improved flow control.

Also in 2006, during the Unit 1 recovery an internal inspection of the 1-FCV-74-66 valve

was performed. Following this inspection, the 1-FCV-74-66 valve was refurbished and

the valve stem was replaced. However, this valve maintenance was performed using an

out-dated valve drawing, 0-A-12337-M-1E, and inadequate maintenance procedure for

valve internal assembly removal and reinstallation, MCI-0-74-VLV008. This procedure

and applicable drawings did not specify appropriate details for the disassembly of the

disc, stem, and skirt; installation of the disc locking key, modified skirt, and modified

stem; and overall correct design configuration of the valve. During the 2006 valve stem

replacement, the stem disc thrust washer was not installed, the disc-to-skirt joint was not

welded to specifications, and the installed disc skirt had undersized threads.

The licensees inspection of the valve found the threads on both the disc and upper disc

skirt in generally good condition. However, laboratory microscopic analysis indicated

beaking or rollover of disc skirt thread crowns. Laboratory analysis of the disc-to-skirt

welds also found that the welds were significantly undersized (i.e., a 0.20 inch fillet

versus 0.50 inch fillet) with general porosity and cracking. The licensees root cause

analysis of the stem and disc separation was still in progress at the end of the inspection

period.

The licensee had identified evidence of multiple impact strikes on the FCV-74-66 valve

disc from the blunt end of the separated stem. The inspectors found this to be evidence

pointing to how long the disc may have been separated from the stem because during

plant operations, the valve was only cycled during quarterly surveillance testing. The

inspectors concluded that FCV-74-66 was incapable of performing its safety function for

longer than its TS 3.5.1 allowed outage time (AOT) of seven days. As part of their root

cause analysis, the licensee was attempting to determine a more exact failure time and

duration in order to better evaluate the resultant safety significance. The last time Unit 1

RHR Loop II was successfully placed in-service, thereby demonstrating FCV-74-66 was

still operable, was on March 12, 2009 for shutdown cooling.

Analysis: The inspectors determined that the licensees failure to establish adequate

design control and perform adequate maintenance on the Unit 1 outboard LPCI injection

valve, 1-FCV-74-66, which resulted in the valve being left in a significantly degraded

condition and RHR loop II unable to fulfill its safety function, was a performance

deficiency. This performance deficiency was considered greater than minor because it

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was associated with the Protection Against External Factors attribute of the Reactor

Safety/ Mitigating Systems Cornerstone and adversely affected the cornerstone

objective of ensuring availability and reliability of systems designed to respond to

initiating events to prevent undesirable consequences. Specifically, the RHR subsystem

was rendered incapable of being aligned to perform its safe shutdown function due to

the failure of 1-FCV-74-66. The inspectors assessed the finding using Inspection

Manual Chapter (IMC) 0609, Significance Determination Process (SDP), and determined

the finding was potentially greater than very low safety significance because it adversely

affected the operators ability to achieve safe shutdown. Since this finding was

potentially greater than Green it will require a Phase 3 SDP assessment. The safety

characterization of this finding is not yet finalized and is currently characterized as To Be

Determined (TBD). This finding does not have a cross-cutting aspect because it is not

reflective of current licensee performance.

Enforcement: Technical Specification LCO 3.5.1, ECCS-Operating, in part, required that

each RHR subsystem shall be operable in Modes 1, 2 and 3, with an allowed outage

time of 7 days, or place the unit in Hot Shutdown (Mode 3) within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Cold

Shutdown (Mode 4) within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Contrary to the above, between March 13, 2009,

and October 23, 2010, the Loop II RHR subsystem was inoperable without the licensee

taking the required TS actions. Pending determination of safety significance, this finding

is identified as an apparent violation: AV 05000259/2010005-01, RHR Subsystem

Inoperable Beyond the Technical Specifications Allowable Outage Time.

(2) Introduction: A Green self-revealing non-cited violation (NCV) of Unit 1 RHR TS LCO

3.6.2.3, Suppression Pool Cooling, was identified for the licensees failure to comply with

the LCO required actions for an inoperable RHR suppression pool cooling subsystem.

Description: On October 27, 2010, the 1C RHR pump motor seized while Loop I was in

operation for shutdown cooling. Unit 1 was in Mode 5 with reactor vessel water level

greater than 23 above the flange, fuel pool gates open, and the auxiliary decay heat

removal (ADHR) in-service. Operators promptly started the 1A RHR pump to restore

shutdown cooling flow. The Loop II of RHR was OOS for repairs. Approximately three

hours later, operators secured the 1A RHR pump for outage work and declared the

ADHR system as the TS required system for core cooling.

The 1C RHR pump had been in-service for shutdown cooling for approximately 94 hours0.00109 days <br />0.0261 hours <br />1.554233e-4 weeks <br />3.5767e-5 months <br />

prior to experiencing a catastrophic failure of the motor on October 27. Total service

time for the 1C RHR pump since November 2007 was approximately 350 hours0.00405 days <br />0.0972 hours <br />5.787037e-4 weeks <br />1.33175e-4 months <br />. The

mission time of the 1C RHR pump to perform its intended safety functions was 30 days

(i.e., 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />). Consequently, the 1C RHR pump had been incapable of meeting its

required mission time, and thereby considered inoperable, since at least November

2007.

The inspectors found that as part of the Unit 1 recovery project, the 1A and 1C RHR

Loop I pump motors were sent offsite to the licensees Power Service Shop (PSS) in

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June 2004 to be refurbished. In March of 2005, the refurbished and reassembled 1C

RHR pump motor experienced excessive vibration during no-load run testing by PSS. In

August 2005, the motor was disassembled, inspected, bearings replaced, reassembled

and no-load tested again but vibration readings remained unacceptably high. In

September 2005, the 1C RHR pump motor was field balanced, no-load tested

acceptably, and returned to Browns Ferry. During uncoupled and coupled runs of the

1C RHR pump motor in September to October 2006, the licensee identified elevated iron

content in the lower motor bearing oil reservoir which was indicative of internal motor

wear (e.g., rubbing between stationary and rotating elements). This reservoir was

subsequently flushed on five separate occasions over a six week period due to

persistently elevated iron content in the oil which turned the oil completely black. Almost

immediately upon return to service (RTS) in 2007, the IC RHR pump motor exhibited an

increasing trend of high vibration as determined by the Predictive Maintenance Program.

Unit 1 was restarted on May 17, 2007.

After the Unit 1 restart, until October 2010, the 1C RHR pump motor continued to exhibit

an ever increasing trend of elevated radial and axial vibrations, and iron content in the

lower bearing oil reservoir. The inspectors concluded that these persistent symptoms

were indicative of internal wear that went undiagnosed by the licensee. From March

2009 through August 2010, four PERs and two WOs were initiated to specifically

address and correct the degraded equipment conditions associated with high motor

vibrations. The licensees initial diagnosis concluded the 1C RHR pump motor was

unbalanced and needed to be re-balanced. However, all four PERs were closed to two

WOs (initiated in March and August 2009) which were never worked. Both WOs were

removed and/or rejected from the daily work week schedule and the most recent U1R8

outage.

Subsequent disassembly, inspection, and root cause evaluation determined that the

rotor of the 1C RHR pump motor had come into physical contact with the stator which

resulted in mechanical seizure of the motor. The direct cause of the motor seizure was

due to a dynamic physical bow in the rotor shaft, compounded by the field balance

weights, which resulted in a significant loss of air gap between the rotor and stator when

the motor was in operation. This led to internal rubbing over approximately four years

which resulted in catastrophic mechanical failure of the motor. The licensee attributed

the root cause of this failure to a misdiagnosis of the dynamic rotor bow that was treated

as a rotor imbalance problem during the PSS motor refurbishment in 2005.

The inspectors identified that the 1C RHR pump motor performance over the past four

years provided evidence that the rotating elements of the motor (i.e., rotor assembly)

had been rubbing against the stationary elements (i.e., stator, upper/lower bearing air

and oil seals, and lower bearing). The inspectors concluded that the licensees

predictive maintenance and corrective action programs failed to adequately recognize,

evaluate and/or understand an adverse trend in elevated iron content of the lower

bearing oil reservoir and increased axial and radial vibrations that exceeded their alert

levels for the 1C RHR pump.

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Analysis: The inspectors determined that the licensees misdiagnosis and failure to

correct a dynamic physical bow in the 1C RHR pump motor rotor constituted a

performance deficiency that resulted in a degraded condition which directly led to

mechanical failure of the 1C RHR motor. This performance deficiency was considered

greater than minor because it was associated with the Mitigating Systems cornerstone

and adversely affected the equipment performance objective to ensure the availability

and capability of the RHR system to respond to initiating events to prevent undesirable

consequences (i.e., core damage). Specifically, the 1C RHR subsystem was degraded

to the point that it was incapable of performing its intended safety functions for the

required mission time. Since the 1C RHR motor failure occurred during Mode 5

shutdown conditions after a significant period of shutdown cooling operation, the finding

was evaluated according to IMC 609, Appendix G, Shutdown Operations SDP,

Attachment 1, Phase 1 Operational Checklists, Checklist 7, Refueling Operation with

Reactor Coolant Level Above 23. Accordingly, the finding was determined to be of very

low safety significance (Green) because the 1A RHR pump and the ADHR system were

available, when only one RHR pump was needed per Section I.C of Checklist 7.

The cause of this finding was directly related to the cross cutting aspect of Thorough

Evaluation of Identified Problems in the Corrective Action Program component of the

Problem Identification and Resolution area, because the licensee did not adequately

evaluate the precursors related to the degraded 1C RHR pump motor performance and

properly prioritize the resolution of a known condition adverse to quality in time to

preclude motor failure P.1(c).

Enforcement: The RHR TS LCO 3.6.2.3, Suppression Pool Cooling, in part, required

that four RHR suppression pool cooling subsystems shall be OPERABLE in Modes 1, 2

and 3, with an allowed outage time of 30 days, or place the unit in Hot Shutdown (Mode

3) within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Cold Shutdown (Mode 4) within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Contrary to the above,

between November 2007 and October 2010, the 1C RHR suppression pool cooling

subsystem was inoperable without the licensee taking the required TS LCO actions.

However, because the finding was determined to be of very low safety significance

(Green) and has been entered into the licensees CAP as PER 274840, this violation is

being treated as an NCV consistent with the Enforcement Policy. This NCV is identified

as NCV 05000259/2010005-02, Degraded 1C RHR Pump Motor Rendered One RHR

Subsystem Inoperable Beyond the Technical Specifications Allowable Outage Time.

.2 Unit 3 Forced Shutdown Due To Main Generator Exciter High Bearing Vibrations

a. Inspection Scope

On December 26, 2010, Unit 3 commenced a forced shutdown due to high vibrations on

the main generator/exciter bearings. The main control room received an alarm for high

vibrations and noticed two locations (bearings #11 and #12) had experienced a sudden

step change in vibrations that exceeded the turbine trip setpoint. The operators initiated

a manual reactor scram, followed by a trip of the main turbine, as required by their

operating procedures. The licensee initiated necessary repairs to the affected bearings

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and the main generator exciter. The licensee determined the cause of the high

vibrations was due to a high temperature difference between the 3A and 3B exciter

coolers that resulted in reduced clearances between the exciter casing and bearing

housings. Unit 3 remained shutdown through the end of the report period. During this

short notice forced outage, the inspectors examined the conduct of critical outage

activities pursuant to TS, applicable procedures, and the licensees outage risk

assessment and outage management plans. The more significant outage activities

witnessed, monitored, examined and/or reviewed by the inspectors were as follows:

  • Shutdown and cooldown of Unit 3 in accordance with general operating instruction

(GOI) 3-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and

Reduction in Power During Power Operations, and 3-SR-3.4.9.1(1), Reactor Heatup

and Cooldown Rate Monitoring

  • Outage risk assessment and management
  • Control and management of forced outage and emergent work activities

Corrective Action Program

The inspectors reviewed PERs generated during the Unit 3 forced outage and verified

that initiation thresholds, priorities, mode holds, and significance levels were assigned as

required.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed portions and/or reviewed completed test data for the following

five surveillance tests of risk-significant and/or safety-related systems to verify that the

tests met TS surveillance requirements, UFSAR commitments, and in-service testing

and licensee procedure requirements. The inspectors review confirmed whether the

testing effectively demonstrated that the SSCs were operationally capable of performing

their intended safety functions and fulfilled the intent of the associated surveillance

requirement.

In-Service Tests:

  • 2-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate

Test at Rated Reactor Pressure

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Routine Surveillance Tests:

  • 0-SR-3.8.4.4 (SB-D), Shutdown Board D Battery Modified Performance Test

Test

Reactor Coolant System Leak Detection Tests:

  • 3-SR-3.4.5.3, Drywell Floor Drain Sump Flow Integrator Calibration

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP7 Emergency Exercise Evaluation

a. Inspection Scope

On December 14, the inspectors observed the Emergency Preparedness (EP) portion of

a site exercise consistent with the requirements of NRC Inspection Procedure

711114.07. The inspectors observed emergency response operations in the simulated

control room to verify that event classification and notifications were done in accordance

with EPIP-1, Emergency Classification Procedure and other applicable Emergency Plan

Implementing Procedures. The inspectors also attended the licensees critique of the

drill to verify any inspector observed weaknesses were also identified by the licensee.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

Cornerstone: Initiating Events

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and

reporting the Performance Indicators (PIs) listed below, including procedure NPG-

SPP-02.2, Performance Indicator Program. The inspectors examined the licensees PI

data for the specific PIs listed below for the fourth quarter of 2009 through the third

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quarter of 2010. The inspectors compared the licensees raw data against graphical

representations and specific values reported to the NRC for the third quarter 2010 PI

report to verify that the data was correctly reflected in the report. Additionally, the

inspectors validated this data against relevant licensee records (e.g., PERs, Daily

Operator Logs, Plan of the Day, Licensee Event Reports, etc.), and assessed any

reported problems regarding implementation of the PI program. Furthermore, the

inspectors met with responsible plant personnel to discuss and go over licensee records

to verify that the PI data was appropriately captured, calculated correctly, and

discrepancies resolved. The inspectors also used the Nuclear Energy Institute (NEI) 99-

02, Regulatory Assessment Performance Indicator Guideline, to ensure that industry

reporting guidelines were appropriately applied.

  • Unit 1 Unplanned Scrams with Complications
  • Unit 2 Unplanned Scrams with Complications
  • Unit 3 Unplanned Scrams with Complications

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Review of items entered into the Corrective Action Program:

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees CAP. This review was accomplished by reviewing daily Service Request (SR)

report summaries, and periodically attending Corrective Action Review Board (CARB)

and PER Screening Committee (PSC) meetings.

.2 Semiannual Review to Identify Trends

a. Inspection Scope

As required by Inspection Procedure 71152, the inspectors performed a review of the

licensees CAP implementation and associated documents to identify trends that could

indicate the existence of a more significant safety issue. The inspectors review included

the results from daily screening of individual PERs (see Section 4OA2.1 above),

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licensee trend reports and trending efforts, and independent searches of the PER

database and WO history. The review also included issues documented outside the

normal CAP in system health reports, corrective maintenance WOs, component status

reports, site monthly meeting reports and maintenance rule assessments. The

inspectors review nominally considered the six-month period of July 2010 through

December 2010, although some PER database and WO searches expanded beyond

these dates. The inspectors reviewed the licensees integrated trend review (ITR)

program and the quarterly implementation of the process as documented in licensee

procedure NPG-SPP-02.8, Integrated Trend Review, Rev. 01. Furthermore, the

inspectors verified that adverse or negative trends identified in the licensees PERs,

periodic reports and trending efforts were entered into the CAP. Inspectors interviewed

the appropriate licensee management and also reviewed new procedures, NPG-SPP-

02.8, Integrated Trend Review, Rev. 01 and NPG-SPP-02.7 PER Trending, Rev. 01

issued during this period.

b. Findings and Observations

No findings were identified, but the inspectors did identify a number of observations as

discussed below.

The purpose of the licensees integrated trend review process was to identify the top

issues (gaps to excellence) requiring management attention. Other objectives of the ITR

program were to provide status of the top issues and their progress to resolution, identify

continuing issues, emerging trends and issues to be monitored, review progress towards

resolving past top issues, review issues identified by external organizations such as the

NRC, INPO, Nuclear Safety Review Board (NSRB), QA, etc., and determine why they

were not identified by line organizations. The inspectors determined that the new

guidance provided in NPG-SPP-02.8 was adequate to meet the purpose and objectives

of the ITR program. The inspectors also reviewed the two most recent Integrated Trend

(IT) reports. The licensee had identified certain departments that did not submit their

reports on time which contributed to the site report being issued after its required due

date. The inspectors noted that SRs were written for each occurrence. The inspectors

also noted that the new procedures improved the consistency of trend discussions and

the report format across departments.

The inspectors also identified several other observations related to the licensees

implementation of the ITR program. The licensee initiated PER 302232 for these

observations.

The inspectors conducted an independent review to identify potential adverse trends,

and identified several notable trends which were either verified to be in the licensees

CAP and/or referred to the licensee who entered them into their CAP. The potential

adverse trends were as follows:

  • During the Unit 1 refueling outage (RFO) U1R8, the inspectors noted four service

requests (SR) were written to document foreign material in the Unit 1 spent fuel pool

(SFP). The licensee initiated SR 281642 and PER 282539 to address several

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additional examples of foreign material in the SFP and reactor vessel. The license

initiated PER 277764 to document the adverse trend in foreign material during the

U1R8 RFO. As foreign material issues were discovered, SRs were initiated and

appropriate corrective actions taken to remove the foreign material and provide

personnel coaching where appropriate. Additional actions to review and/or improve

the implementation of the sites foreign material exclusion (FME) program were

planned, but not completed by the end of this inspection period.

  • PER 213116 was generated to address the licensees actions to address an

inspector identified trend, concerning the adequacy of post maintenance testing

(PMT), which has been previously documented in multiple inspection reports, but is

yet to be adequately addressed by the corrective action program. The licensee

developed another corrective action plan including actions to develop a PMT team

with a team charter. The inspectors reviewed the charter which included additional

actions for the team. However, due dates for those actions were not provided. The

PER was closed on July 22, 2010, upon development of the team charter. The

licensee identified the corrective actions from PER 213116 were not effective and

initiated PER 246534 on Aug. 25, 2010. This PER was assigned a higher level in

accordance with licensee procedure NPG-SPP-02.8. None of the corrective actions

were completed by the end of this inspection period. On Dec. 17, 2010, the

inspectors observed the PMT associated with the U2 HPCI system. It was

discovered that two additional work orders (WO) for the HPCI system did not have

PMTs assigned. The licensee captured this issue in their CAP as PER 299877.

  • The inspectors identified a potential adverse trend regarding inaccuracy and

incomplete information contained in LERs. During the review of LERs from 2009

through 2010, inspectors identified seven examples where LERs contained

inaccurate statements, incomplete descriptions and details, and other technical and

editorial errors. The licensee had previously initiated the following PERs to resolve

the issues identified by the inspectors: PERs 215479, 205308, 201410, and 163176.

Additionally, as documented in report Section 4OA3.1 below, the inspectors

identified two violations associated with inadequate and incomplete information in

Unit 3 LER 2009-003. The licensee initiated SR 314177 to address this apparent

adverse trend.

  • Over the past operating cycle, Units 2 and 3 have developed a large number of

control rod Rod Position Indication System (RPIS) component problems. Unit 2 had

outstanding WOs on about 25 different control rods with RPIS related problems, and

Unit 3 had about 15 control rods with WOs. These problems involved incorrect back

lighting, intermittent drift alarms, and primarily inaccurate rod position indication at

one or more positions. The licensee initiated SRs 313460 and 313465 to address

this adverse trend.

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.3 Annual Sample: Review of Cross Cutting Aspect H.2.c

a. Inspection Scope

The inspectors reviewed the cause analysis and specific corrective actions associated

with PER 228347, Emerging Trend in Human Performance Cross-Cutting Area. This

PER was initiated to evaluate an overall adverse trend in NRC findings and licensee

events attributed to human performance issues associated with the Resources

component area (i.e., H.2) defined by Inspection Manual Chapter (IMC) 0310,

Components Within The Cross Cutting Areas. During this inspection, the inspectors

focused primarily upon the cross-cutting aspect (CCA) of H.2.c. In IMC 310, this CCA is

described as the licensee ensures that personnel, equipment, procedures, and other

resources are available to assure nuclear safety, specifically, those necessary for

complete, accurate, and up-to-date design documentation, procedures, and work

packages, and correct labeling of components. Within the preceding 12 months, the

NRC has cited three violations with a cross-cutting aspect of H.2.c that were included as

part of PER 228347. The violations for which the CCA is cited include: Failure to

perform an adequate risk assessment during severe weather conditions (PER 171402);

Inadequate operating procedures cause partial loss of reactor feedwater, which results

in Unit 2 manual reactor scram (PER 203538); and Inadequate surveillance procedure to

ensure all relevant RPV metal temperatures were monitored during leak testing (PERs

223539 and 224778). The licensee also included an additional 57 PERs for review in

the common cause analysis of this PER. The inspectors reviewed the events and

analysis of the events, the extent of condition, previous similar events, root and

contributing causes, the licensees safety culture evaluation, and corrective actions

taken or planned for this PER.

b. Findings and Observations

No findings were identified. Inspectors determined that, in general, the licensees root

cause analysis (RCA) of the human performance cross cutting implications of the NRC

findings associated with the H.2.c CCA was technically accurate, of sufficient depth, and

consistent with the licensees process. The RCA was determined to have adequately

addressed operability, reportability, common cause, generic concerns, extent-of-

condition, and extent-of-cause. The inspectors also determined that the licensee had

appropriately identified and prioritized corrective actions. Furthermore, in general, the

corrective actions to prevent recurrence (CAPRs) and additional corrective actions

implemented to date, or scheduled to be implemented, are considered reasonable to

address the root cause. However, the inspectors identified the following observations

which were discussed with the licensee:

Not all of the licensees corrective actions were completed. As part of the licensees

corrective actions, various communication methods of management expectations have

been ongoing. Training teams were formed or forming, and industry benchmarking was

in progress. The plant procedure upgrade was also in progress and lists of the most

difficult procedures for each department have been generated. However, after these

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more difficult procedures were identified it was unclear as to what actions the licensee

was taking to ensure personnel and management were taking any compensatory actions

regarding future use of these procedures until the planned improvements were

implemented. In response to the inspectors observations, PER 302263 was initiated to

evaluate whether some form of compensatory measures should be established when

working with these procedures.

In addition, the licensee had identified prior similar events related to human performance

through self assessments, benchmarking and QA assessments. However, previous

corrective actions related to these prior events had failed to provide sustainable

resolution of the issues in the past. Since the licensees corrective actions for the H.2

adverse trend were still ongoing, a final effectiveness review of these actions has not

been accomplished. The inspector noted that in the interim, since the licensee identified

this adverse trend, and began taking corrective actions; there have been no new NRC

findings or violations with a CCA of H.2.c.

.4 Annual Follow-up of Selected Issues - Assessment of Progress in Addressing the

Substantive Cross-Cutting Issue (SCCI)

a. Inspection Scope

The inspectors reviewed the licensees progress on the development and

implementation of corrective actions to address the SCCI identified in the NRC Annual

Assessment Letter for the period of January - December 2009. The SCCI was identified

in the problem identification and resolution area, in the aspect of thorough evaluation of

identified problems (P.1 (c)). The SCCI was subsequently held open in NRC Mid-Cycle

Performance Review Letter for the period January - July 2010 in order to give the

licensee time to develop and schedule a corrective action plan. This PI&R inspection

was the first opportunity to review the licensees actions to address the open SCCI.

The inspectors conducted a detailed review of the licensees common cause and root

cause analysis (PER 223536) related to the open SCCI to assess the adequacy of the

licensees evaluation of the problems identified. The inspectors reviewed these

evaluations against the guidance in licensee procedure NPG-SPP-03.1.6, Root Cause

Analysis and the performance attributes of NRC Inspection Procedure 71152. The

inspectors assessed if the licensee had adequately determined the cause(s) of identified

problems, and had adequately addressed operability, reportability, common cause,

generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if

the licensee had appropriately identified and prioritized corrective actions to prevent

recurrence. Inspectors also reviewed a sample of completed corrective actions (twenty-

five of fifty-two total corrective actions were complete at the time of the inspection) to

independently verify that the corrective actions were implemented as intended.

The inspectors also noted that the licensee had identified a trend of findings in the

problem identification and resolution area, in the aspect of timely corrective actions

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(P.1 (d)) which they included in their root cause analysis and corrective actions to

address the open SCCI. Because of the inclusion of both cross cutting areas in their

root cause analysis and corrective actions, the observations of the inspectors reflect the

licensees progress in addressing both areas. Documents reviewed are listed in the

Attachment.

b. Assessment

Inspectors determined that, in general, the licensees evaluation of the SCCI was

technically accurate and of sufficient depth to address the issue. The analysis was

determined to have adequately addressed operability, reportability, common cause,

generic concerns, extent-of-condition, and extent-of-cause. The inspectors also

determined that the licensee had appropriately identified and prioritized corrective

actions. However, the inspectors did make the following observations regarding the

licensees evaluation of the SCCI (for which the licensee initiated PER 311304):

  • Inspectors noted that many of the actions identified to address the open SCCI were

similar to previous corrective actions to address weaknesses in the Problem

Identification and Resolution area (PERs 151140, 153438 and 136489) that had

proven to be ineffective over the long term. Inspectors also noted that previous

corrective actions (CA) included the actions taken to address weaknesses in the

area of timeliness of corrective actions for the P.1(d) SCCI closed out in NRC Mid-

Cycle Performance Review Letter for the period January - July 2009. The licensees

discussion of previous similar events included in the root cause report noted that

previous corrective actions had been unsuccessful at ensuring sustainable

improvements. However, a rigorous evaluation of why previous actions were

ineffective was not included.

  • Inspectors noted that clearly defined success measures were not defined for the

critical aspects of all of the corrective actions to prevent recurrence (CAPRs)

identified in the root cause as required by licensee procedure PIDP-6, Root Cause

Analysis. Most notably, no success measures were defined in the root cause to

measure the critical aspect of sustainability of the CAPRs. Inspectors concluded

that, given the history of unsustainable corrective actions to address weaknesses in

the Problem Identification and Resolution area noted in the root cause, additional

success measures and effectiveness review actions were warranted to ensure

sustainable and effective corrective actions.

Inspectors determined that, in general, the corrective actions implemented to date or

scheduled to be implemented to address the SCCI were appropriate. The licensee

initiated CAPRs and additional corrective actions to address the three common causes

identified. The inspectors were able to evaluate the implementation of a sample of the

twenty-five completed corrective actions. During the review of selected records, the

inspectors identified two corrective actions which were not completely implemented as

intended, as follows:

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  • CA 223536-039 was created as an Interim Corrective Action to address the Extent of

Cause (EOC) for the root cause. This action directed the CARB to reevaluate all

open root cause PERs to determine if the following were adequately addressed:

plant risk significance, timeliness of actions, and sufficiently detailed and timely

interim actions. The action was closed to a previously completed action from a

different PER, CA 214592-010, which was completed five months earlier. However,

inspectors identified that the scope of the completed action only included PERs

greater than one year old. The licensee initiated SR 294998 to address this issue.

  • CA 223536-023 directed a backwards assessment of RCAs and ACEs for systems

important to safety for the previous two years to verify the adequacy of the previous

evaluations and CAs. The CA also directed an increase in sample size if necessary.

A contractor conducted the backwards assessment for the licensee and provided the

results in a report dated September 2, 2010. The licensee subsequently marked the

CA as complete. Inspectors reviewed the report and noted that it documented

eleven separate issues for immediate follow-up out of a sample of seven RCEs and

thirty-one ACEs reviewed. However, at the time of the inspection, 3 months after the

report was completed, the issues had not been evaluated and no consideration was

given to increasing the sample size based on the number issues identified. The

licensee initiated SR 295007 to address this issue.

Inspectors were unable to assess the effectiveness of the completed and open

corrective actions due to the number of open corrective actions and the limited time

since implementation of completed corrective actions.

c. Findings

No findings were identified.

4OA3 Event Follow-up

.1 (Closed) Licensee Event Reports (LERs) 05000296/2009-003-01 and -02, Reactor Core

Isolation Cooling System Inoperable Longer Than Allowed By the Technical

Specifications

a. Inspection Scope

The original LER 50-296/2009-003-00 dated May 24, 2010, and applicable PERs

200183,119628 and 246527, including cause determination and corrective action plans,

were reviewed by the inspectors and documented in Section 4OA3.2 of NRC inspection

report (IR) 05000296/2010003. As a result of this prior review, two violations of NRC

requirements were identified: NCV 05000296/2010003-02, Unit 3 RCIC System

Inoperable beyond the Technical Specifications Allowed Outage Time; and NCV

05000296/2010003-03, Failure to Provide Complete and Accurate Information in LER

0500296/2009-003-00. The NCV 05000296/2010003-03 was the result of the review of

the original LER, when the inspectors determined that, contrary to 10 CFR 50.9, LER

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0500296/2009-003-00 was not accurate or complete in all material aspects for which the

licensee initiated PER 246527. Specifically, the LER inaccurately reported the duration

of system inoperability, inaccurately reported the availability of HPCI while the RCIC was

inoperable, and did not report a previous event that occurred on the same unit with the

same cause as required by 10 CFR 50.73(b)(5).

As part of the PER 246527 corrective actions, the licensee issued a revised LER

0500296/2009-003-01 on July 15, 2010. The principal intent of this LER revision was to

establish the date that began the period of RCIC inoperability as March 22, 2006, and to

notify the NRC that additional time was needed to complete a determination of any

concurrent HPCI system inoperability. The licensee revised their commitment to

supplement the LER to September 30, 2010. Subsequently, the licensee issued their

second revised LER 0500296/2009-003-02 on August 31, 2010. This LER was revised

by the licensee to correct and update the LER narrative with an expanded timeline and

results from their efforts to retrieve high speed computer data regarding actual RCIC

pump performance. This second revision was also intended to address and correct any

missing or inaccurate information identified by the inspectors in the original LER. This

revised LER included changes to the Abstract, Description of Event, Cause of the Event,

Analysis of the Event, and Corrective Actions.

The second revision of the LER did specifically report a more accurate duration of

system inoperability, including when the nonconforming turbine electric governor-remote

(EG-R) had been installed; a discussion of concurrent HPCI unavailability while RCIC

was inoperable; and a discussion of the previous event on February 9, 2007 that

occurred on the same unit with the same cause. The inspectors reviewed the revisions

1 and 2 of the LERs, and verified the root causes and previously identified corrective

actions for the RCIC flow instabilities were not substantially different, except for the

additional clarifying information provided.

b. Findings

This LER is considered closed with one NRC identified finding related to the LER itself.

Introduction: A Severity Level IV, cited violation (VIO) of 10 CFR 50.9, Completeness

and Accuracy of Information, was identified by the inspectors for the licensees repeat

failure to provide complete and accurate information regarding the licensees LER

0500296/2009-003-02, Reactor Core Isolation Cooling System Inoperable Longer than

Allowed by Technical Specifications.

Description: Following the Unit 3 reactor scram on August 24, 2009, the RCIC system

auto-initiated as designed and injected into the reactor pressure vessel (RPV) restoring

reactor water level. Subsequent review of RCIC system operating parameters revealed

an unexpected level of instability in system flow and turbine control system response.

The RCIC system flowrate was discovered to have oscillated between approximately

300 gpm to 900 gpm. On September 12, 2009, Unit 3 conducted a shutdown for

unrelated maintenance and the RCIC EG-R hydraulic actuator was replaced. The

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licensee had the EG-R vendor conduct testing and inspection of the original EG-R to

determine the cause of the oscillations. The vendor determined that the cause of the

oscillations was due to a missing buffer piston and buffer spring in the EG-R. These

components were essential in providing the smoothing and/or dampening function of the

controller, without which resulted the observed flow oscillations. It was determined that

the EG-R was missing these components since original installation in 2006. On March

25, 2010, the licensee determined that the installation of this EG-R had rendered the

Unit 3 RCIC system inoperable which represented a condition prohibited by TS since

RCIC had been inoperable beyond the AOT of TS LCO 3.5.3. In addition, Unit 1 had

changed modes of operation without evaluating the impact on risk as required by TS

3.0.4.

On May 24, 2010, the licensee submitted LER 05000296/2009-003-00. The LER

attributed the root cause for the RCIC flow oscillations to be the missing EG-R

components. However, the LER did not mention when the faulty EG-R had been

installed. Also, this LER inaccurately stated that RCIC had been inoperable from August

26, 2009, to September 12, 2009, and that HPCI was operable during this time period.

Furthermore, the LER failed to identify and describe the reactor scram event on

February 9, 2007 when the Unit 3 RCIC flow oscillations were first recognized, and did

not describe the subsequent corrective actions. The corrective actions following this

event included maintenance on a control system wiring terminal lug, EG-R needle valve

adjustment and turbine governor valve replacement. However, the subsequent post

maintenance testing was conducted using the routine quarterly surveillance procedure

which operated RCIC in a condensate storage tank (CST) recirculation mode, rather

than aligned for RPV injection. Since no RCIC oscillations were identified during the

surveillance test, the licensee erroneously concluded that the flow oscillations had been

corrected. Unbeknownst to the licensee the faulty EG-R only became a factor when

RCIC was actually injecting against the dynamic pressure head of the RPV. The

inspectors determined that, contrary to 10 CFR 50.9, the initial LER 0500296/2009-003-

00 was not accurate or complete in all material aspects for the reasons mentioned

above. The licensee then initiated PERs 232668 and 246527 and the NRC documented

a non-cited violation (i.e., NCV 05000296/2010003-03).

Subsequently, the licensee issued revised LERs 05000296/2009-003-01 on July 15,

2010, and 05000296/2009-003-02 on August 31, 2010. The inspectors reviewed the

revised LERs, and identified incomplete and inaccurate information in LER

0500296/2009-003-02. The inspector identified issues are detailed below:

  • Section 5 Event Date was incorrectly documented as August 26, 2009. The event

date was March 22, 2006, following the replacement of the RCIC EG-R as

documented by the licensee in the cover letter of the first LER revision.

  • Section I referenced time is not specific for when the licensee had actually

determined the RCIC had been previously inoperable which was March 25, 2010,

significantly distanced from the event date.

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  • The narrative, Sections II, IV and VI, discussed the previous RCIC instability event

on February 9, 2007, but failed to describe the corrective actions taken to address

the RCIC oscillations (i.e., maintenance activities and post maintenance testing) that

proved unsuccessful but led the licensee to conclude via a functional evaluation that

the RCIC system was operable. Furthermore, the narrative did not describe why

these repairs and subsequent post maintenance testing did not resolve the RCIC

instabilities. The licensees business procedure BP-213, Managing TVAs Interface

With NRC, established the required guidance for writing and submitting LERs. This

guidance directed the licensee to utilize NUREG-1022, Event Reporting Guidelines

10 CFR 50.72 and 50.73. Section 5.2.5, Previous Occurrences, of NUREG-1022

states that if any earlier events, in retrospect, were significant in relation to the

subject event to discuss why prior corrective action did not prevent recurrence. This

same omission by the licensee, and the specific NUREG-1022 guidance, was

documented in detail as part of NCV 05000296/2010003-03.

  • The narrative,Section IV, Analysis of the Event, incorrectly referenced oscillations

that occurred on February 9, 2007 as occurring on February 13, 2007.

  • The narrative,Section V, Assessment of Safety Consequences, while discussing

periods of coincident HPCI unavailability with RCIC being inoperable, did not

address the resultant TS impacts to Unit 3.

  • The narrative,Section VII.B, Previous LERs on Similar Events, indicated no similar

events. However, NUREG 1022 states that previous similar events are not

necessarily limited to events reported in LERs.

  • The narrative,Section VII.C, Additional Information, referenced the two PERs for the

two separate RCIC flow oscillation events, but does not reference a PER for the

previous 10CFR50.9 NCV for incomplete and inaccurate LER information.

  • The corrective actions established by PERs 232668 and 246527 to develop and

submit another LER revision that would address the inaccurate and incomplete

information, specifically documented in IR 05000296/2010003 for NCV

05000296/2010003-03, were not effective.

The licensee initiated PER 304722 to determine the cause of the inaccurate and

incomplete information contained in revised LER 0500296/2009-003-02, and to evaluate

if the LER should be further supplemented. The licensees guidance for corresponding

with the NRC required multiple levels of supervisory and management review and

concurrence on submittals, including LERs. Despite these multiple levels of review and

previous NRC identification of incomplete or inaccurate information for the original LER

documented in IR 05000296/2010-003, the licensees CAP and LER review process did

not prevent LER revision 2 from again containing inaccurate and incomplete information.

Based on extensive NRC involvement on the issue and previously completed NRC

regulatory action, the inspectors determined that the licensees failure to provide

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complete and accurate information in the LER was not a willful attempt to withhold

information, but rather a break down in the CAP, and LER submittal review and approval

process.

Analysis: Because violations of 10 CFR 50.9 are considered to potentially impede or

impact the regulatory process, they are dispositioned using the traditional enforcement

process. The inspectors concluded that the licensee had reasonable opportunity to

foresee and correct the incomplete/inaccurate information prior to the information being

submitted to the NRC. As a result, this issue was considered a performance deficiency.

The performance deficiency was ultimately considered to be more than minor per the

NRC Enforcement Manual, Section 2.10.F, since adequate corrective action was not

taken to ensure complete and accurate information was provided in LER revision 2, and

this finding was identified by the NRC. Furthermore, because the violation was NRC

identified and repetitive, this violation was dispositioned as a cited violation in

accordance with Section 2.3 of the NRC Enforcement Policy and Section 3.1.2 of the

NRC Enforcement Manual, and determined to be of Level IV significance based on

Section 6.9 of the NRC Enforcement Policy. No cross cutting aspect was assigned

because the ROP was not applicable.

Enforcement: 10 CFR 50.9, Completeness and Accuracy of Information, required, in

part, that information provided to the Commission by a licensee shall be complete and

accurate in all material respects. Contrary to the above, on August 31, 2010, the

licensee submitted a revised LER, as corrective action for a previous 10 CFR 50.9

violation involving the inoperability of the Unit 3 RCIC system, which was not complete

and accurate in all material respects. Specifically, the revised LER did not report the

correct event date, did not discuss prior corrective actions (e.g., maintenance and

testing) for a previous event, and why these corrective actions did not prevent

recurrence (as specifically documented in IR 05000296/2010003). This violation was

determined to be a Severity Level IV violation and was entered into the licensees

corrective action program as PER 304722. This is a violation of 10 CFR 50.9 and is

identified as VIO 05000296/2010005-03, Repeated Failure to Provide Complete and

Accurate Information in LER 0500296/2009-003-02. A notice of violation is attached.

.2 (Closed) LER 05000260/2010-003-00, Reactor Scram Due to Closure of the Main Steam

Isolation Valves and Subsequent Invalid RPS Scram from the Intermediate Range

Monitoring System

a. Inspection Scope

On June 9, 2010, Unit 2 experienced an automatic reactor scram from full power due to

an unexpected closure of the main steam isolation valves (MSIV) from a Primary

Containment Isolation Signal (PCIS) Group 1 actuation. The inspectors initial event

followup and evaluation of this event were documented in Section 4OA3.1 of IR

05000260/2010003. Since then, the inspectors reviewed the associated LER dated

August 9, 2010. Following completion of the root cause analysis, the licensee was

unable to determine a definitive cause for this event. However, two possible causes

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were identified: 1) Foreign material from the control air system might have caused the

2A (MSIV) direct current (DC) solenoid valve to bind; or 2) Intermittent electrical fault in

the DC power system. Although neither of these possible causes were confirmed, the

licensee developed corrective actions to address both of them.

b. Findings

No findings were identified. This LER is considered closed.

.3 (Closed) LER 05000260/2010-001-00, Condition Prohibited By Technical Specifications

When Two Emergency Core Cooling Systems, Loops I and II of the Residual Heat

Removal System Low Pressure Coolant Injection System, Became Inoperable

a. Inspection Scope

The inspectors reviewed LER 50-260/2010-001, dated April 26, 2010, and the applicable

PER 218493, including associated apparent cause determination and corrective action

plans.

On February 25, 2010, operators determined that Unit 2 had entered TS Limiting

Condition of Operation (LCO) 3.0.3 when both loops of RHR were declared inoperable.

Within an hour of entering TS LCO 3.0.3, operators began reducing reactor power to

shutdown Unit 2 as required by TS. However, once operators realigned the ECCS keep

fill system to increase RHR Loop II system pressure, they were able to declare RHR

Loop II operable again. At which point, TS LCO 3.0.3 was exited and reactor power was

returned to 100 percent the same day. Unit 2 had entered TS LCO 3.0.3 for

approximately 80 minutes due to both loops of RHR being inoperable. The conditions

that led up to both loops of RHR being declared inoperable are described below.

On December 18, 2009, Operational Decision Making Issue (ODMI) 210437 was issued

to address RHR system Loop II discharge piping elevated temperatures due to reactor

coolant seat leakage past the RHR Loop II injection line discharge check valve and gate

valve. This ODMI established monitoring guidelines and specific temperature thresholds

for ensuring RHR Loop II discharge piping remained sub-cooled to preclude steam

voiding. On February 24, 2010, RHR system Loop I was removed from service for

planned maintenance. Then on February 25, operators recognized that RHR Loop II

discharge temperature had increased to 264° Fahrenheit (F) which exceeded the ODMI

trigger value (i.e., 260°F) for ensuring operability. However, per the ODMI instructions,

operators were able to promptly lineup an alternate keep fill source that increased RHR

Loop II discharge pressure which restored sub-cooled conditions.

Subsequent engineering evaluation by the licensee, determined that the actual ODMI

trigger value was indeed conservative for the actual RHR Loop II discharge piping

temperatures and keep fill pressure. This evaluation was able to conclude that the

elevated RHR Loop II discharge temperatures of February 25 had not reached steam

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saturation conditions. Furthermore, an ultrasonic testing (UT) examination of the RHR

Loop II discharge piping on February 26 confirmed the absence of any steam voiding.

Based on the licensees evaluation, and UT exam, the RHR system Loop II was fully

operable and capable of performing its intended safety functions on February 25, 2010.

b. Findings

No findings were identified. This LER is considered closed.

.4 Unit 3 Manual Reactor Scram

a. Inspection Scope

On December 26, 2010, Unit 3 was manually scrammed from approximately 90% power

due to high vibrations on the main generator exciter bearings that exceeded the required

threshold for tripping the main turbine. Upon notification by the shift manager, the

inspector responded to the control room and verified that the unit was stable in Mode 3

(Hot Shutdown), and confirmed that all safety-related mitigating systems had operated

properly. The inspector evaluated safety equipment and operator performance before

and after the event by examining existing plant parameters, strip charts, plant computer

historical data displays, operator logs, and the critical parameter trend charts in the

reactor scram report. The inspector also interviewed available onshift Operations

personnel, examined the implementation of the applicable ARPs and AOIs, including 3-

AOI-100-1, Reactor Scram, and reviewed the written notification made in accordance

with 10 CFR 50.72. The inspector discussed the preliminary cause of the bearing high

vibrations with responsible Operations personnel.

b. Findings

No findings were identified during the initial event followup.

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4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings

No findings were identified.

.2 (Closed) Unresolved Item (URI) 05000259, 260 and 296/2010004-01, Uncontrolled

Materials Adversely Impacted the Capability of the EDG Building Emergency Drainage

System to Mitigate an Internal Flooding Event

a. Inspection Scope

This URI 05000259, 260 and 296/2010004-01 was opened pending additional

information from the licensee and subsequent review by the inspectors. The licensee

initiated PER 256390 to remove the temporary equipment from the Unit 1/2, and Unit 3,

EDG building lower corridors. The inspectors reviewed the licensees actions and

conducted tours of the EDG buildings to verify whether all temporary equipment was

removed or properly restrained per the licensees procedural requirements. Additionally,

the inspectors reviewed the results of WOs 111530751 and 111530754 to verify the as-

found condition of the EDG building floor drain sumps were operable, and whether the

building sump high level alarm would alert the main control room. The licensee also

initiated PER 268624 to perform a past operability evaluation of the EDG building

emergency drain function which considered the potential adverse impacts of the specific

items left in the EDG building lower corridors. Furthermore, the inspectors reviewed the

licensees annunciator response procedures (ARP) for a high water level in the DG

building sump to verify whether required operator actions would be timely and sufficient

to prevent an adverse impact to the EDGs from an internal flooding event.

b. Findings

No findings were identified. However the inspectors identified a minor violation of TS

5.4.1.a because the licensee failed to implement the requirements of licensee procedure

0-TI-471, Temporary Equipment Control, Rev. 04 in the common U1/2 EDG building

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and U3 EDG building. TS 5.4.1.a required, in part, that written procedures shall be

established, implemented, and maintained covering the activities and procedures

recommended in Regulatory Guide (RG) 1.33, Rev. 2, Appendix A. Section 1c, of RG

1.33, Rev. 2, Appendix A required the licensee to have a procedure for Equipment

Control. Licensee procedure, 0-TI-471, Temporary Equipment Control, section 7.1.1

required temporary equipment to be removed from plant areas; or, attended, restrained

or stored. Contrary to the above requirements, the inspectors identified unattended and

loose materials in the EDG building lower corridors that included potential licensing basis

internal flooding sources (e.g., the EECW North and South supply header piping). This

failure to comply with TS 5.4.1.a constitutes a violation of minor significance that is not

subject to enforcement action in accordance with the NRCs Enforcement Policy.

.3 (Closed) Notice of Violation (VIO) 07200052/2010-003-01 (EA-10-215), Repeated

Failure to Control Transient Combustibles in Proximity of the Independent Spent Fuel

Storage Facility (ISFSI)

a. Inspection Scope

The inspectors reviewed the licensees response to VIO 07200052/2010-003-01 (EA-10-

215) dated November 29, 2010. The licensees corrective actions included

establishment of an ISFSI Pad Escort Zone (i.e., fenced in area of the ISFSI pad) with

appropriate posted signage and gate locks to preclude unattended vehicles from being

parked on the pad and to require Operations escort for any access to the ISFSI pad.

The licensee also established an ISFSI Pad Exclusion Zone (i.e., an area 150 feet from

any point on the ISFSI pad) that would be routinely monitored by Operations to ensure

transient combustibles were maintained at least 150 feet from the ISFSI pad.

The inspectors conducted a tour of the ISFSI Pad Escort Zone and ISFSI Pad Exclusion

Zone to verify the licensees controls were in place and were being effectively applied.

The inspectors also reviewed the ISFSI Pad Protection Plan instructions and briefing

sheet guidance contained in the latest BFN Operations Daily Instructions (ODI) dated

December 15, 2010. Furthermore, the inspectors reviewed the latest revision (revision

210) of 0-GOI-300-1, Operator Round Logs, Attachment 12, Outside Operator Round

Log, Sections 6.0, Steps (23) and (24), that define and verify the ISFSI Pad and

Exclusion Zones are clear of uncontrolled transient combustibles.

b. Findings

No findings were identified. This VIO is considered closed.

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.4 Follow-up On Alternative Dispute Resolution Confirmatory Orders (IP 92702)

a. Inspection Scope

During the inspection period the inspectors completed a review of TVAs completion of

Confirmatory Order for Office of Investigation Report Nos. 2-2006-025 & 2-2009-003,

item numbers 2, 5, 7, 8, and 9. These individual items are considered closed.

2. By no later than seven (7) calendar days after the issuance of this Confirmatory

Order, a member of TVAs executive management responsible for the licensees

nuclear power plant fleet will, in writing, communicate TVAs policy, and the

expectations of management, regarding the employees rights to raise concerns

without fear of retaliation in the context of this Confirmatory Order.

5. By no later than sixty (60) calendar days after the issuance of this Confirmatory

Order, representatives from the TVAs OGC and Human Resources shall conduct a

lessons learned training session

7. TVA shall incorporate a discussion of NRCs employee protection rule in the next

revision of the One Team, One Fleet, One TVA booklet. The next revision will be

completed by no later than December 31, 2010.

8. By no later than ninety (90) calendar days after the issuance of this Confirmatory

Order, TVA shall modify its contractor in-processing program to ensure that a TVA

representative provides a presentation regarding the CRP program and the TVAs

SCWE policy during the contractor in-processing sessions.

9. By no later than ninety (90) calendar days after the issuance of this Confirmatory

Order, TVA shall revise its training program for new supervisors to incorporate a

classroom discussion of the NRCs employee protection rule and the Companys

policy on SCWE.

The inspectors also performed a follow-up review of TVAs implementation of

Confirmatory Order for Office of Investigation Report Nos. 2-2006-025 & 2-2009-003,

item numbers 1, 6, and 10. These items are not closed.

1. By no later than ninety (90) calendar days after the issuance of this Confirmatory

Order, TVA shall implement a process to review proposed licensee adverse

employment actions at TVAs nuclear plant sites before actions are taken to

determine whether the proposed action comports with employee protection

regulations, and whether the proposed actions could negatively impact the SCWE.

6. Through calendar year 2013, TVA shall conduct Town Hall-type meetings at least

annually at its nuclear power plants and corporate office with TVA and contractor

employees which address topics of interest, including a discussion on TVAs policy

regarding fostering a SCWE.

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10. TVAs annual online computer-based training course initiative, which discusses the

components of a nuclear safety culture, what is meant by a SCWE, and the avenues

available to raise concerns, shall be maintained through calendar year 2013.

b. Findings and Observations

No findings were identified.

The inspectors raised a concern during the inspection of item #1 about the content of

TVA's Adverse Employment Action Procedure - TVA-SPP-11.10. TVA staff understood

the concern and were in the process of incorporating modifications to the procedure with

an expected completion of late February or early March 2011.

4OA6 Meetings, Including Exit

.1 Exit Meeting Summary

On January 11, 2011, the senior resident inspector presented the inspection results to

Mr. Keith Polson and other members of the sites staff, who acknowledged the findings.

All proprietary information reviewed by the inspectors as part of routine inspection

activities were properly controlled, and subsequently returned to the licensee or

disposed of appropriately.

An exit meeting was conducted on October 15, 2010, to discuss the findings of the

71111.11B inspection. The inspectors confirmed that no proprietary information was

reviewed during this inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Enclosure 1

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Albright, Simulator Manager

S. Austin, Licensing

W. Baker, Operations Support Superintendent

S. Bono, Maintenance Manager

J. Boyer, System Engineering Manager

O. Brooks, Operations LOR Supervisor

W. Byrne, Site Security Manager

P. Chase, Site Nuclear Assurance Manager

J. Colvin, Engineering Programs Manager

P. Donahue, Assistant Engineering Director

G. Doyle, Assistant to the Site Vice President

M. Durr, Director of Engineering

M. Ellet, Maintenance Rule Coordinator

J. Emens, Licensing Manager

B. Evans, Instrumentation and Controls Superintendent

A. Feltman, Emergency Preparedness Manager

N. Gannon, Plant General Manager

K. Gregory, Director Projects

K. Groom, Mechanical Design Engineering Supervisor

B. Jones, Mechanical Maintenance Superintendent

J. Keck, Reactor Engineering Manager

S. Kelly, Assistant Work Control Manager

R. King, Design Engineering Manager

D. Malinowski, Operations Training Manager

T. Marlow, Director of Safety and Licensing

M. McAndrew, Assistant Operations Manager

O. Miller, Operations Manager

J. Morris, Director Training

R. Norris, Radiation Protection Manager

W. Nurnberger, Work Control Manager

W. Pearce, Performance Improvement Manager

K. Polson, Site Vice President

M. Rasmussen, Operations Superintendent

T. Smith, Component Engineering Manager

J. Underwood, Chemistry Manager

S. Walton, Electrical Maintenance Superintendent

D. Zielinski, Operations Training

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000259/2010005-01 AV RHR Subsystem Inoperable Beyond the TS

Allowed Outage Time (Section 1R20.1(1))05000296/2010005-03 VIO Repeated Failure to Provide Complete and

Accurate Information in LER 0500296/2009-003-02

(Section 4OA3.1)

Opened and Closed

05000259/2010005-02 NCV Degraded 1C RHR Motor Rendered One RHR

Subsystem Inoperable Beyond the TS Allowed

Outage Time (Section 1R20.1(2))

Closed

07200052/2010-003-01 VIO Repeated Failure to Control Transient

Combustibles in Proximity of the Independent

Spent Fuel Storage Facility (Section 4OA5.3)

05000296/2009-003-01 LER Reactor Core Isolation Cooling System Inoperable

Longer Than Allowed By the Technical

Specifications (Section 4OA3.1)

05000296/2009-003-02 LER Reactor Core Isolation Cooling System Inoperable

Longer Than Allowed By the Technical

Specifications (Section 4OA3.1)

05000260/2010-003-00 LER Reactor Scram Due to Closure of the Main Steam

Isolation Valves and Subsequent Invalid RPS

Scram from the Intermediate Range Monitoring

System (section 4OA3.2)

05000260/2010-001-00 LER Condition Prohibited By Technical Specifications

When Two Emergency Core Cooling Systems,

Loops I and II of the Residual Heat Removal

System Low Pressure Coolant Injection System,

Became Inoperable (section 4OA3.3)

05000259, 260, 296/2010004-01 URI Uncontrolled Materials Adversely Impacted the

Capability of the EDG Building Emergency

Drainage System to Mitigate an Internal Flooding

Event (Section 4OA5.2)

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

3

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 2 (Section

4OA5.4)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 5 (Section

4OA5.4)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 7 (Section

4OA5.4)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 8 (Section

4OA5.4)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 9 (Section

4OA5.4)

Discussed

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 1 (Section

4OA5.4)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 6 (Section

4OA5.4)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 10 (Section

4OA5.4)

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

0-GOI-200-1, Freeze Protection Inspection, Rev. 66

Operating Logs

0-AOI-100-3, Flood Above Elevation 558, Rev. 33

MPI-0-260-DRS001, Inspection and Maintenance of Doors, Rev. 38

MPI-0-000-INS001, Inspection of Flood Protection Devices, Rev. 12

SPP-10.14, Freeze Protection, Rev. 0

0-GOI-200-1, Freeze Protection Inspection, Revs. 64, 65, 66

SR 271672

PER 272691

SR 288551

PER 289066

WO 110821237 - Perform Inspection of the Diesel Bldg Flood Protection Portable Bulkheads

WO 06-714206-000 - Perform Inspection of the Diesel Bldg Flood Protection Portable

Bulkheads

WO 08-713109-000 - Perform Inspection of the Diesel Bldg Flood Protection Portable

Bulkheads

FPDQ (Freeze Protection Report), RFP-NWM117, dated 11/2/2010

WO # 01-011443-001, Generate Report

WO # 05-725438, Duct Heater

WO # 08-710085-000, D/G Heaters

WO # 09-725938-000, D/G Space Heater

WO # 09-726137-000, Strip Heater

WO # 110980907, RCW A Drain Valve

WO # 111300432, Expansion Tank Safety Valve

WO # 111361895, ADHR Instrumentation Heaters

WO # 111537776, RHRSW Pump B1

WO # 111581385, EECW Strainer Valve

SR # 271610, EECW Strainer Valve

SR # 277461, Freeze Protection GOI

SR # 277480, RHRSW Tunnel Doors

SR # 277481, Cancel WO

PER # 277476, Freeze Protection GOI

PER # 277482, RHRSW Tunnel Doors

PER # 277484, Cancel WO

BFN Operations Log, 11/6/2010 Midnight Shift, 11/7/2010 Day Shift

44N267, Diesel Generator Building Personnel Access Doors Portable Bulkhead, Rev. A

3-47W587-1, Standby Diesel Gen Bldg Unit 3, Mechanical Drains & Embedded Piping, Rev. 3

3-47W587-2, Standby Diesel Gen Bldg Unit 3, Mechanical Drains & Embedded Piping, Rev. 2

0-47E851-4, Flow Diagram Drainage, Rev. 13

Section 1R04: Equipment Alignment

0-OI-72, Auxiliary Decay Heat Removal System, Rev. 48

0-OI-72, ADHR System, Attachment 1, Valve Lineup Checklist, Eff. Date 11-10-2009

0-OI-72, ADHR System, Attachment 2, Panel Lineup Checklist, Eff. Date 7-14-2006

0-OI-72, ADHR System, Attachment 3, Electrical Lineup Checklist, Eff. Date 5-04-2010

0-OI-72, ADHR System, Attachment 2, Instrument Inspection Checklist, Eff. Date 11-12-2007

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

5

FSAR 10.22 Auxiliary Decay Heat Removal System (ADHR)

3-OI-82, Standby Diesel Generator System, Rev. 99

3-OI-82/ATT-1D, Standby Diesel Generator 3D Valve Lineup Checklist, Rev. 96

3-OI-82/ATT-2D, Standby Diesel Generator 3D Panel Lineup Checklist, Rev. 96

3-OI-82/ATT-3D, Standby Diesel Generator 3D Electrical Lineup Checklist, Rev. 95

3-OI-82/ATT-4D, Standby Diesel Generator 3D Instrument Inspection Checklist, Rev. 96

FSAR 8.5 Standby AC Power Supply and Distribution

3-OI-75, Core Spray System, Rev. 50

3-OI-75, Attachment 1, Core Spray System Valve Lineup Checklist, Eff. Date 8-28-09

3-OI-75, Attachment 2, Core Spray System Panel Lineup Checklist, Eff. Date 4-08-08

3-OI-75, Attachment 3, Core Spray System Electrical Lineup Checklist, Eff. Date 8-28-09

3-47E814-1, Core Spray System Flow Diagram, Rev. 34

0-47E873-1, -2, Flow Diagram Aux Decay Heat Removal System, Sheet 1 & 2, Date 7-12-97

0-47E610-72-1, -2, Control Diagram Aux Decay Heat Removal System, Sheet 1 & 2, Date 7-12-97

0-15E900-1, Electrical Instrument Details, Date 8-6-97

0-15E740-1, Single-Line Diagram ADHR Service Entrance and MCC, Date 7-12-97

Section 1R05: Fire Protection

Fire Protection Report, Volume 1, Fire Protection Plan, Units1/2/3, Rev. 8

Fire Protection Report, Volume 1, Fire Hazards Analysis, Units1/2/3, Rev. 8

Fire Protection Report, Volume 2, Sections IV.7, Pre-Plan No. RX3-519, Rev. 7

Fire Protection Report, Volume 2, Sections IV.8, Pre-Plan No. RX3-519, Rev. 7

Fire Protection Report, Volume 2, Sections IV.8, Pre-Plan No. RX3-565, Rev. 7

Fire Protection Impairment Permit #s; 09-1920

Fire Watch Route/Coverage Sheet: Permit/Route #: Reactor Bldg. & Turbine Bldg, 10/16/10 to

10/18/10

TVAN Fire Watch Briefing and Turnover Form: Permit/Route #: U1, 2, &3 RX/TB Bldg, Multiple

Sheets from 10/16/10 to 10/18/10

SR 268995

SR267561

SR267696

SR267624

SR267677

SR267630

Fire Protection Report, Volume 2, Sections IV.13, Pre-Plan No. DG3-565, Revision 8

Fire Protection Report, Volume 2, Sections IV.13, Pre-Plan No. DG3-583, Revision 8

Fire Protection Report, Volume 1, Fire Hazards Analysis, Units1/2/3, Rev. 8

Fire Protection Report, Volume 1, Fire Protection Plan, Units1/2/3, Rev. 8

Section 1R08: Inservice Inspection Activities

GE-UT-511, Procedure for the Automated Examination of Core Spray Piping Welds Contained

within the Reactor Pressure Vessel, Revision 7

N-PT-9, Liquid Penetrant Examination of ASME and ANSI Code Components and Welds,

Revision 0034

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

6

N-UT-64, Generic Procedure for the Ultrasonic Examination of Austenitic Pipe Welds, Revision

0011

N-UT-66, Generic Procedure for the Ultrasonic Examination of Weld Overlay Austenitic Pipe

Weld, Revision 0006

N-UT-76, Generic Procedure for the Ultrasonic Examination of Ferritic Pipe Welds, Revision

0007

NETP-112, BWR Reactor Pressure Vessel Internals Inspections (RPVII), Revision 0000

54-ISI-363-05, Remote Underwater In-Vessel Visual Inspection of Reactor Pressure Vessel

Internals, Components, and Associated Repairs in Boiling Water Reactors, Revision

10/21/2008

54-ISI-850-007, Manual Ultrasonic Examination of BWR Reactor Vessel Nozzle Inner Radius

Regions and Nozzle to Shell Welds (inner 15%), Revision 9/7/2010

PDI-UT-6, Generic Procedure for Ultrasonic Examination of Reactor Pressure Vessel Welds,

Revision 3/17/2009

Problem Evaluation Report (PER) 156982, U1C7 Jet Pump Restrainer Bracket Indication

PER 275955, Indications found on Core Spray Downcomer A, Weld P4a

PER 275958, Lost Quals after being requalified

PER 277618, U1R8 Jet Pump Wedge Wear and Set Screw Gaps/Indications

Report #: 0801464.401.R0, BFNP Unit 1 Cracked Jet Pump Set Screw Tack Welds Evaluation

Report #: BFN1-01-JLCJ2, Browns Ferry Nuclear Power Station- Unit 1 Core Spray Piping

Ultrasonic Examination

Section 1R11: Licensed Operator Requalification

TRN-11.4, Continuing Training for Licensed Personnel, Rev. 16

SPP-10.0, Plant Operations, Rev. 05

OPDP-1, Conduct of Operations, Rev. 18

Benchmark Tests:

Unit 2 PLU Trip from 100% power 7/8/04

Unit 2 Scram(RFP 2A/2B trip) at 100% power 8/5/05

Unit 3 Power Level Imbalance 12/31/07

Design Changes:

DCR B 1538 (SDCR B1538) "Replace Unit 2 Main Generator Circuit Brown Boveri DR Air Blast

breaker with new ABB SF6 HEC-7 type

General Items Reviewed:

License Reactivation Packages (5).

LORP Training Attendance records (15).

Medical Files (20).

Remedial Training Records (15).

Remedial Training Examinations (15).

Feedback Summaries (50).

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

7

License Event Reports (LER):

LER 50-259/2009-001-00, Turbine Trip and Reactor Scram Due to Power Load Unbalance

Signal on Main Generator (2/18/2009)

LER 50-259/2009-002-00, Unexpected Logic Lockout Of The Loop II Residual Heat Removal

System Pumps (3/21/2009)

LER 50-259/2009-003-00, A Train Standby Gas Treatment System Inoperable Longer Than

Allowed by The Technical Specification (6/19/2009)

LER 50-259/2009-004-00, High Pressure Core Injection Found Inoperable During Compensate

Header Level Switch Calibration and Functional Test (7/24/2009)

LER 50-260/2009-001-00, Manual Reactor Scram following Stator Cooling Water Equipment

Failure (2/16/2009)

LER 50-260/2009-007, Manual Scram During Removal of a Reactor Feedwater Pump from

Service

LER 50-260/2009-002-01, Leak In An ASME Class 1 Code Reactor Pressure Boundary Pipe

(05/21/2009

LER 50-260/2009-003-00, Main Steam Relief Valve As found Setpoint Exceeded Technical

Specification Lift Pressure (6/9/2009)

LER 50-260/2010-003, Reactor Scram Due to Closure of the Main Steam Isolation Valves and

Subsequent Invalid RPS Scram From the Intermediate Range Monitoring System (6/9/2010)

LER 50-260/2010-001, Condition Prohibited by Technical Specifications, (2/25/2010)

LER 50-260/2010-002, Failure to Meet the Requirement of Technical Specification Limiting

Condition for Operation Due to Inoperable Primary containment Isolation Instrumentation

LER 50-260/2010-004, HPCI Isolation During Time Delay Relay Calibration (6/16/2010)

LER 50-260/2010-005, High Pressure Coolant Injection System Isolation Experienced During

Performance of High Pressure Coolant Isolation Steam Supply Low Pressure Functional Test

(7/12/2010)

LER 50-269/2010-001, Safety relief Valves As-Found Setpoints Exceeded Technical

Specification Lift Pressure Values (4/20/1010)

LER 50-269/2010-002-00, A Subsystem of the Standby Liquid Control System was Inoperable

Longer than Allowed by the Plants Technical Specification (4/20/2010)

LER 50-269/2010-003-01, Multiple Test Failures of Excess Flow Check Valves (3/26/2010)

Malfunction Tests:

Condensate Pump Trip (FW01) completed 9/4/09

Loss of Condenser Vacuum (OG02) Completed 9/18/09

RCIC Low Suction Pressure Turbine Trip (RC03 Completed 9/27/09)

JPM Packages:

JPM 231 Operator 1 Manual Actions 0-SSI-16

JPM 249 Control Room Abandonment Attachment 4 Part A

JPM 224 Transfer of 480V HVAC Board B Power Supplies

JPM 238 Operator 3 Manual Actions 0-SSI-1-1

Unit 2 Simulator Information:

Transient #1 Manual Scram Completed 8/26/09

Transient #2 Simultaneous Trip of all Feed Pumps Completed 8/26/09

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

8

Transient #3 Simultaneous Closure of all MSIVs Completed 8/26/09

Transient #4 Simultaneous Trip of all Recirc Pumps Completed 8/26/09

Transient #5 Single Recirc Pump Trip Completed 8/26/09

Transient #6 Turbine Trip < 30% Power Completed 8/26/09

Transient #7 Manual Rate Power Ramp Completed 8/26/09

Transient #8 Max Size LOCA with LOOP Completed 8/26/09

Transient #9 Max Size Unisolable Main Steam Line Rupture Completed 8/26/09

Transient #10 MSIV Isolation and Relief Valve Failure Completed 8/26/09

100% Steady State Test Completed 8/26/09

75% Steady State Test Completed 8/26/09

50% Steady State Test Completed 8/26/09

Stability Test (Drift) Completed 8/26/09

Real Time Test Completed 8/26/09

Written Examination Reviewed:

Requal Written SRO exams for weeks 2 and 5 of 2009.

Section 1R12: Maintenance Effectiveness

Cause Determination Evaluation (CDE) 750, CS System I Logic Power Functional Failure

CDE 823, 1B CS Room Cooler Fan Functional Failure

CDE 867, 1B CS Room Cooler Low EECW Flow 1/28/09

CDE 864, 1B CS Room Cooler Low EECW Flow 2/09/09

CDE 862, 1B CS Room Cooler Low EECW Flow 9/13/09

CDE 852, 1B CS Room Cooler Low EECW Flow 11/19/09

CDE 897, 1B CS Room Cooler Low EECW Flow 2/17/10

CDE 925, 1B CS Room Cooler Functional Failure Due to Low EECW Flow

CDE 835, Unit 2 CS I Unavailable Due to Elevated Fluid Temperature 10/05/09

CDE 863, 2B CS Room Cooler Low EECW Flow

CDE 880, 2D CS Pump Breaker Functional Failure

CDE 881, Unit 2 CS I Unavailable Due to Elevated Fluid Temperature 1/10/10

CDE 836, 3EA Shutdown Board Loss of Control Power Functional Failure

FSAR Section 6.4.3 Core Spray System, BFN-23.3

OPL171.045 License Operator Training, Core Spray System, Rev. 11

PER 209302, Core Spray Venting

PER 219100, 3A CS and 3A RHR Room Cooling Coils Not Meet Original Specifications

PER 221650, U3 Core Spray Piping Indications Re-Inspection

PER 227894, Re-Status of CS Systems to (a)(1)

PER 236909, 1B CS Room Cooler Failed

PER 238523, CS II Room Cooler Testing Weekly

Technical Specifications and Bases 3.5.1 ECCS-Operating, Amendment 249 and Rev. 50

respectively

Units 1, 2, and 3 Function 75-B Core Spray (a)(1) Plan, Rev 0, Effective Date 6/29/10

WO 10569918, Replacement of Unit 1 Testable Check Valve 75-26

WO 10569919, Replacement of Unit 3 Testable Check Valve 75-26

WO 110717766, 3A CS Pump Oil Change Due to ISO Particle Count

WO 110714652, 3C CS Pump Oil Change Due to ISO Particle Count

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

9

WO 110874232, CS 75-53 Metal Particles in Motor Clutch Housing

WO 110900580, 3A CS Pump Cyclone Separator Tubing Against Pedestal

BFPER940777, Recirculation Pump 2B Discharge Valve Failure to Close

BWROG-TP-09-005, Inspection of Motor Operated Valve Limitorque AC Motors with

Magnesium Rotors, Rev. 0

Flowserve Technical Update 06-01, Reliance Motors/Magnesium Rotors, dated December 26,

2006

Flowserve Technical Update 08-01, Reliance Motors/Magnesium Rotors, dated December 19,

2008

GE SIL 425, EQ Test Anomalies of Reliance Motors in Limitorque Valve Operators, Rev. 1

NRC Information Notice 86-02: Failure of Valve Operator Motor During Environmental

Qualification Testing, dated November 20, 2006

NRC Information Notice 2006-26: Failure of Magnesium Rotors in Motor-Operated Valve

Actuators, dated November 20, 2006

PER 95431, Failure of 3-MVOP-68-77

PER 95610, PM Program for Magnesium Rotor Motors

PER 95611, Motor Start Attempts

PER 98884, Predictive Monitoring of Reactor Recirc Motors

PER 940777, GE SIL 425

PER 162116, MOV Users Group Inspection Guidance

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

PRA Evaluation Response BFN-0-10-114, Revs 0 and 1

Unit 1 Operator Work Around #1-072-OWA-2010-0135, Alternate Makeup to Secondary Basin

for ADHR B Primary Heat Exchanger Leak

Unit 1 ORAM Safety Function Status reports dated October 28, 2010

Operator chronological logs for October 28, 2010

Unit 1 ORAM Safety Function Status reports dated October 26, 2010

Operator chronological logs for October 26, 2010

Section 1R15: Operability Evaluations

BFN Operators Log for October 4 through 6, 2010

Design Criteria BFN-50-7082, Standby Diesel Generator, Rev. 13

EMD-ESI Diesel Generator Owners Group, Lube Oil Issue and Guidance Document, Rev. 1,

January, 2006

EMD-ESI Diesel Generator Owners Group, Operating Practice Guidance: Loss of Circulating

and/or Turbocharger/Soak Back Oil Pump, Revised April 2006

FSAR Section 8.5, Standby AC Power Supply and Distribution, BFN-23

Licensed Operator Lesson Plan OPL171.038, Diesel Generators and Standby Auxiliary Power

Systems, Rev. 14

Operating Instruction 3-OI-82, Standby Diesel Generator System, Rev. 99

Operator Workaround 3-082-OWA-2010-0124, 3-TS-82-7B Diesel Generator 3B Immersion

Heater Temperature Switch has failed

PER 260536, DG 3EB TS-82-7B Immersion Heater Temperature Switch Not Controlling

Properly

Technical Specifications and Bases 3.8.1, AC Sources - Operating, Amendment 215

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

10

Unit 3 Reactor Building Operator Rounds for October 1 through 7, 2010

PER 209288

PER 254463

PER 2710558

SR 269892

SR 92821

WO 08-712742-001,

WO 09-710550-000

Functional Evaluation, B Diesel Generator Loading Limitation PER 209288, 254463, SR 269892

0-OI-82, Standby Diesel Generator System, Rev. 112

0-SR-3.8.1.1(B), Diesel Generator B Monthly Operability Test, Rev. 45

0-SR-3.8.1.7(B), Diesel Generator B 24 Hour Run, Rev. 17

FSAR Section 8.5

Tech Spec 3.8.1

Prompt Operability for C3 EECW Pump (PER 257317)

WO 111031504, BFN-0-PMP-023-0091 [C3 EECW Pump] Packing Replacement

EECW Pump Shaft Evaluation by OEM dated October 6, 2010

WO: 111530751

WO: 111530754

PER 268624

Diesel Generator Building Emergency Drain Piping Past Operability Evaluation, PER 268624

PER 256390

SR 263466

SR 263491

0-TI-471, Temporary Equipment Control, Rev. 04

1-ARP-9-7C, Annunciator Response Procedure Panel 9-7, Rev. 21

3-ARP-9-7C, Annunciator Response Procedure Panel 9-7, Rev. 31

1-ARP-9-20A, Annunciator Response Procedure Panel 1-9-20, Rev. 29

PER 178142

Functional Evaluation 43661, Rev. 4

Operator Work Around (OWA) 0-082-OWA-2009-0095

SR 73153

SR 230938

PER 244607

PER 217659

WO-09-720120-001

2-BFN-RTP-082, Restart Test Program for the Standby Diesel Generators, Rev. 0

2-BFN-RTP-082, Restart Test Program for the Standby Diesel Generators, Rev. 1

2-BFN-RTP-082, Restart Test Program for the Standby Diesel Generators, Rev. 2

BFN-50-7082, Detailed Design Criteria Document Standby Diesel Generator, Rev. 15

BFN-50-7200E, Detailed Design Criteria Document 4kV AC Auxiliary Power System, Rev. 12

Drawing: 0-45E724-1, Wiring Diagram 4160V Shutdown BD A Single Line, Rev. 26

0-AOI-57-1A, Loss of Offsite Power (161 and 500kV)/Station Blackout, Rev. 77

PER 255823, Holtec cask FSAR information insufficient to ensure MPC-68 loaded per analysis

assumptions.

Functional Evaluation for PER 255823, Rev. 0

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

11

Functional Evaluation Quality Review Grading Sheet, PER 255823, Dated 11/02/2010

SR 254930, Holtec cask MPC-68

Holtec Document ID 1031135, dated 9-23-2010

Holtec Document ID 1031137RI dated 10-27-2010

Holtec FSAR, Rev. 2

Holtec Technical Specification Bases, Rev. 7

Section 1R18: Plant Modifications

1-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate Test, Rev. 4

SR 301210, CILRT Procedure Enhancement

PER 302266, CILRT Procedure Enhancement

NPG-SPP-06.3, Pre-/Post-Maintenance Testing, Rev. 0

SPP-9.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 8

1-SR-3.3.5.1.2 (ATU A), Core and Containment Cooling Systems Analog Trip Unit Functional

Test, Rev. 4

1-SR-3.3.5.1.2 (ATU B), Core and Containment Cooling Systems Analog Trip Unit Functional

Test, Rev. 5

1-SR-3.3.5.1.2 (ATU C), Core and Containment Cooling Systems Analog Trip Unit Functional

Test, Rev. 4

1-SR-3.3.5.1.2 (ATU D), Core and Containment Cooling Systems Analog Trip Unit Functional

Test, Rev. 3

DWG 1-45E670-2, Wiring Diagrams, ECCS Div. I Analog Trip Units Schematic, Rev. 3

DWG 1-45E670-8, Wiring Diagrams, ECCS Div. II Analog Trip Units Schematic, Rev. 3

BFN-VTD-AG01-0060, AGASTAT, Nuclear Qualified Control Relays, Rev. 0

NEI 96-07, Guidelines for 10 CFR 50.59 Implementation, Rev. 1

Section 1R19: Post-Maintenance Testing

0-OI-72, Auxiliary Decay Heat Removal System, Rev. 48

0-OI-72, ADHR System, Attachment 1, Valve Lineup Checklist, Eff. Date 11-10-2009

0-OI-72, ADHR System, Attachment 2, Panel Lineup Checklist, Eff. Date 7-14-2006

0-OI-72, ADHR System, Attachment 3, Electrical Lineup Checklist, Eff. Date 5-04-2010

0-OI-72, ADHR System, Attachment 2, Instrument Inspection Checklist, Eff. Date 11-12-2007

FSAR 10.22 Auxiliary Decay Heat Removal System (ADHR)

WO# 110989877, Connect two diesel generators to the ADHR MCC

WO# 224816-001, Electrical Capacity Determination needed for the ADHR D/G.

EPI-0-072-ADR001, Installation of Feeder Cables for Alternate Supply From Backup Diesel

Generator for ADHR in Support of Refueling Outages, Rev. 12

Calculation Number EDN000072201000002, Sizing ADHR Backup Diesel Generator, Rev. 0

0-SR-3.6.4.3.2(B VFTP), Standby Gas Treatment Filter Pressure Drop and In-Place Leak Tests

- Train B

PER 266981 Secondary Containment Breach not Identified

PER 267418 RCA Boundary in SBGT Building not in Proper Place

PER 267490 Inadequate PMT for WO 111543852

PER 268312 0-DMP-65-503 Found Twisted

PER 268557 Two WO 111543852 Discrepancies

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

12

WO 111543852, Repair of 0-DMP-65-503

1-SR-3.6.1.3.5(RHR II), RHR System MOV Operability Loop II, Rev. 7, dated 11/14/10

1-SR-3.3.3.1.4(H II), Verification of Remote Position Indicators for RHR System II Valves, Rev.

2, dated 11/15/10

ECI-0-000-MOV001, Maintenance for Limitorque Motor Operated Valves, Rev. 42

ECI-0-000-MOV009, Testing of Motor Operated Valves Using MOVATS Universal Diagnostic

System (UDS) and Viper 20, Rev. 22

EPI-0-000-MOV001, Electrical Preventive Maintenance for Limitorque Motor Operated Valves,

Rev. 52

MCI-0-000-PCK001, Generic Maintenance Instructions for Valve Packing, Rev. 24

MCI-0-074-VLV008, Residual Heat Removal Motor Operated Valves FCV-74-52 and FCV-74-

66, Maintenance, Rev. 15

WO 09-723979-000, Partial MOVATS 74-66

WO 111569660, 1-FCV-74-66 Troubleshooting of Failure to Pass Flow

WO 111571105, Refurbishment of RHR 1-FCV-74-66

WO 111571764, EM Support of 1-FCV-74-66 Maintenance

WO 111620630, 74-66 Stem-Skirt Weld Build-Up and Re-Thread

Drawing 1-730E915RE, Sheets 11 and 12, Reactor Protection System, Revs. 6 and 5

respectively

FSAR Section 7.2, Reactor Protection System, Amendment BFN-22

SR 272881, Problems with Screws on CR305 Scram Contactors

SR 277297, Minor Package Closure Issues with Scram Contactor Replacements

SR 298856 Overall PMT Process

SR 298862 Oil Seepage WO Not Having PMT

SR 298871 PMT for Sight Glass Signed Prematurely

SR 299098 ECI-MOV009 Not Included in Work Package

SR 299102 MCIs Missing Sign-Offs

Technical Specifications and Bases 3.5.1, ECCS - Operating, Rev. 47

WO 111105764, EM Support for 73-16

WO 04-723582-000, High Point Sight Glass Vent Cleaning

WO 09-723049-000, Tighten Oil Leaks

3-SR-3.5.1.6(CSII), Core Spray Flow Rate Loop II

WO 09-719726-000, CS Minimum Flow Valve (3-FCV-75-37)

WO 110965566, Core Spray Test Return Valve (3-FCV-75-50)

WO 110979949, 3B CS Motor Oil Replacement

WO 110965563, CS Loop Injection Valve (3-FCV-75-53)

WO 110784067, BFN-3-MVOP-075-0037

WO 110984071, BFN-3-MVOP-075-0050

0-47E873-1, -2, Flow Diagram Aux Decay Heat Removal System, Sheet 1 & 2, Date 7-12-97

0-47E610-72-1, -2, Control Diagram Aux Decay Heat Removal System, Sheet 1 & 2, Date 7-12-97

0-15E900-1, Electrical Instrument Details, Date 8-6-97

0-15E740-1, Single-Line Diagram ADHR Service Entrance and MCC, Date 7-12-97

Section 1R20: Refueling and Other Outage Activities

SPP-10.4, Reactivity Management Program, Rev. 09

SR 304778

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

13

1-SR-3.5.1.1(RHRII), RHR System Venting Loop II

2-SR-3.5.1.1(RHR II), RHR System Venting Loop II

Drawing 1-47E811-1, Flow Diagram Residual Heat Removal System, Rev. 25

Drawing 3-A-12337-M-3A, Cast Steel Pressure Seal Angle Valve with Limitorque SMB-5T

Operator (Nuclear) Assembly, Rev. 2

Drawing C-12337-7-3A, Cast Steel Pressure Seal Angle Valve Special Disc Skirt, Rev. 0

Drawing C-12337-8-1, Cast Steel Pressure Seal Angle Valve with Limitorque SMB-5T Operator

& V-Notched Disc Detail of Special Stem, Rev. 0

General Design Criteria Document BFN-50-7074, Residual Heat Removal System, Rev. 20

Operator Logs, 2/18/09 - 3/13/09

PER 271338, 1-FCV-74-66 Valve Failure A Level Root Cause

PER 303097, Units 2 and 3 FE for RHR Outboard Isolation Valves

Sketch Showing Assembled Parts for Conversion to V-Notch Disc, Dated June 5, 1975

Technical Specifications and Bases 3.5.1 ECCS-Operating, Amendment 269 and Rev. 53

respectively

U1R8 PORC Presentation, 1-FCV-74-66 Valve Failure, PER 271338 A Level Root Cause

WO 111569660, 1-FCV-74-66 Troubleshooting of Failure to Pass Flow

WO 06-724612-000, 1-FCV-74-66 Will Not Close-Limit Switches

WO 05-722286-001, 1-MVOP-74-66 Anti-Rotation Device Needs Adjustment

1-SR-3.4.9.1(1), Rector Heatup and Cooldown Rate Monitoring, Rev. 06

SPP-10.4, Reactivity Management Program, Rev. 09

1-SR-3.4.1 (SLO), Reactor Recirculation System Single Loop Operation, Rev. 02

1-SR-3.4.2.1, Jet Pump Mismatch Operability, Rev. 12

1-SR-3.4.3.2, Main Steam Relief Valve Manual Cycle Test, Rev. 02

3-AOI-100-1, Reactor Scram, Rev. 53

3-GOI-100-12A, Unit S/D from Power Ops to Cold S/D, Rev. 47

3-ARP-9-7B, ARP for Panel 9-7, 3-XA-55-7B

Unit 3 Reactor Scram report dated 12/27/2010

Quick Human Error Analysis Tool report dated 12/26/2010

PER 301505

3-SR-3.4.9.1(1), Reactor Heatup and Cooldown Rate Monitoring, Rev. 17

3-GOI-200-2, Primary Containment Initial Entry and Closeout Inspection, Rev. 30

1C RHR Run History from 2006 through 2010

PER 274840, 1C RHR Motor Failure, Root Cause Analysis Report

Operator Chronological Logs from October 23 thru October 28, 2010

PORC Presentation for 1C RHR Motor Failure

Section 1R22: Surveillance Testing

WO 110931892

SR266363

0-SR-3.7.3.2 (HEPA), Control Room Emergency Ventilation System In Place Leak Test

WO 110725406, CREVS in Place Leak Test

Chronological Test Log (CTL) Procedure No. 0-SR-3.7.3.2 (HEPA)

Nucon International, Inc., Acceptance for In-place Testing

Nucon International, Inc., In-place Test Report

Nucon International, Inc., Airflow Capacity and / or Distribution Test Report

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

14

Nucon International, Inc., HEPA Test Raw Data Sheet

Nucon International, Inc., Calibration Certificate

Nucon International, Inc., Qualifications of Nucon Personnel

1-SI-4.7.A.2.a-f, Primary Containment Integrated Leak Rate Test

Calibration Certificates #22694 & 22695, Mass Flow Indicator (Alicat Scientific)

Calibration Certificates #21276 thru 21313, Temperature Detectors (Graftel)

Calibration Certificates #21314 thru 21326, and 23295, Relative Humidity Chambers (Graftel)

Calibration Certificates #09100015, 22724 and 22725, Pressure Detectors (Paroscientific)

SR 299079, EOI-2 Entry

SR 299090, EOI-3 Entry

SR 298907, HPCI Temporary D/P Gage Tubing Rupture

SR 299213, EOI Label Missing On 2-RI-90-24A

Technical Specifications and Bases 3.5.1, ECCS - Operating, Rev. 47

WO # 111255075

3-SR-3.4.5.3, Drywell Floor Drain Sump Flow Integrator Calibration, Rev. 08

NPG-SPP-06.9.1, Conduct of Testing, Rev. 01

PER: 2330701

SR: 276465

0-45E709-1

0-45E710-1

Section 4OA2: Identification and Resolution of Problems

3QFY10 Integrated Trend Report

4QFY10 Integrated Trend Report

PER 285375 Late Site ITR submittal

PER 276796 Late Engineering ITR submittal

PER 276074 Late Operations ITR submittal

PER 277764 FME trend for U1R8

PER 282539 FME issues in the reactor vessel and SFP

SR 277796 FME trend for U1R8

SR 281642 Document SRs and status of FME found during U1R8

SR 277621 FME in U1 SFP

SR 277617 FME in U1 SFP

PER 136489 Cross Cutting issue for untimely corrective actions

Effectiveness Review of PER 136489

PERs 216386, 225844, 204364 177206-005774364, 177206-005774389,147726, 148788.

PER 177206 ACE Grading 092800402

PER 177206 Extension 005769041

PER 177206 Extension request#1

PER 177206 ACE Grading 092680535

LER write up for HPCI 1-PCV-073-0018Crev8 005774357

LER write up for HPCI 1-PCV-073-0018Crev8 005774383

ACE Report for PER 177206 rev6 092650456

Central Labs report (M29-0189 Preliminary results) 005774350

FW PER 177206 ACE Grading [1].doc 005781152

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

15

ACE 177206 rev7 005783907

ACE Report for PER 177206 rev6 005774382

Procedures:

NPG-SPP-03.1, Corrective Actions Program

NPG-SPP-03.1.4, Corrective Action Program Screening and Oversight, Rev. 0001

NPG-SPP-03.1.10, PER Effectiveness Reviews, Rev. 0001

SRs:

SR 294998, PER action 223536-039 closed without performing all actions

SR 295007, Evaluate the Certrec report

PERs:

PER 136489, Cross Cutting issue for untimely corrective actions

PER 138724, Potential negative trend in work practices

PER 147726, Functional Evaluations

PER 151140, Potential negative trend in the cross cutting program corrective action program

PER 153438, Infrequent Reinforcement of High Performance Standards by Managers and

Supervisors

PER 172053, Scheduled item not performed

Section 4OA3: Event Follow-up

PER 200183, RCIC Flow Oscillations during Unit 3 Scram

BFN Unit 3 Technical Specifications and Bases 3.5.3, RCIC System

FSAR Section 4.7, Reactor Core Isolation Cooling System

BFN-50-7071, Design Criteria, Reactor Core Isolation Cooling System, Rev. 15

LER 50-296/2009-003-00, Reactor Core Isolation Cooling System Inoperable Longer Than

Allowed By the Technical Specifications

LER 50-296/2009-003-01, Reactor Core Isolation Cooling System Inoperable Longer Than

Allowed By the Technical Specifications

LER 50-296/2009-003-02, Reactor Core Isolation Cooling System Inoperable Longer Than

Allowed By the Technical Specifications

3-AOI-100-1, Reactor Scram, Rev. 53

3-GOI-100-12A, Unit S/D from Power Ops to Cold S/D, Rev. 47

3-ARP-9-7B, ARP for Panel 9-7, 3-XA-55-7B

Unit 3 Reactor Scram report dated 12/27/2010

Quick Human Error Analysis Tool report dated 12/26/2010

PER 301505

Section 4OA5: Other

BFN Leadership Development 2011 Plan, October 2010

SR 277529 FME in U1 reactor cavity

SR 277541 FME in U1 reactor cavity

PER 278148 FME in U1 reactor vessel

SR 280474 Protected equipment negative trend

PER 280429 ODM 4.18 protected equipment negative trend

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

16

PER 289002 SPP-9.17 Temporary Equipment Control violations

PER 244854 3QFY10 ITR Analysis of Housekeeping Temporary Equipment Control

SR 297502 Temporary Equipment Control

PER 288827 SPP-9.17 Temporary Equipment Control Violations

SR 298856, PMT process

PER 299877, PMT process

PER 213116, PMT not performed

PER 246534, Potential negative trend in the adequacy of PMTs

NPG-SPP-02.7, PER Trending, Rev. 01

TVA's Adverse Employment Action Procedure - TVA-SPP-11.10

One Team, One Fleet, One TVA booklet

NPG-SPP-02.8, Integrated Trend Review, Rev. 01

PER 248347, Emerging Trend in H.2.c

Root Cause Analysis Report PER 228347

PER 215591, Potential substantive cross-cutting issue in PI&R

PER 302263, Comp measure for each Dept. working with most difficult procedures

NPG-SPP-03.1, Corrective Action Program, Rev. 1

NPG-SPP-03.1.6, Root Cause Analysis, Rev. 1

NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 1

NPG-SPP-18.2, Human Performance Program, Rev. 0

NPG-SPP-18.2.2, Human Performance Tools, Rev. 0

CRP-PAN-F-09-001, NPG Focused Self-Assessment Report

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

LIST OF ACRONYMS

ADAMS - Agencywide Document Access and Management System

ADS - Automatic Depressurization System

ARM - area radiation monitor

CAD - containment air dilution

CAP - corrective action program

CCW - condenser circulating water

CFR - Code of Federal Regulations

CoC - certificate of compliance

CRD - control rod drive

CS - core spray

DCN - design change notice

EECW - emergency equipment cooling water

EDG - emergency diesel generator

FE - functional evaluation

FPR - Fire Protection Report

FSAR - Final Safety Analysis Report

IMC - Inspection Manual Chapter

LER - licensee event report

NCV - non-cited violation

NRC - U.S. Nuclear Regulatory Commission

ODCM - Off-Site Dose Calculation Manual

PER - problem evaluation report

PCIV - primary containment isolation valve

PI - performance indicator

RCE - Root Cause Evaluation

RCW - Raw Cooling Water

RG - Regulatory Guide

RHR - residual heat removal

RHRSW - residual heat removal service water

RTP - rated thermal power

RPS - reactor protection system

RWP - radiation work permit

SDP - significance determination process

SBGT - standby gas treatment

SLC - standby liquid control

SNM - special nuclear material

SRV - safety relief valve

SSC - structure, system, or component

TI - Temporary Instruction

TIP - transverse in-core probe

TRM - Technical Requirements Manual

TS - Technical Specification(s)

UFSAR - Updated Final Safety Analysis Report

URI - unresolved item

WO - work order

OFFICIAL USE ONLY - SECURITY RELATED INFORMATION

Attachment