IR 05000259/2022004

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Integrated Inspection Report 05000259/2022004, 05000260/2022004 and 05000296/2022004
ML23037A849
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 02/07/2023
From: Louis Mckown
Division Reactor Projects II
To: Jim Barstow
Tennessee Valley Authority
References
IR 2022004
Download: ML23037A849 (19)


Text

SUBJECT:

BROWNS FERRY NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000259/2022004, 05000260/2022004 AND 05000296/2022004

Dear Mr. Barstow:

On December 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Browns Ferry Nuclear Plant. On January 26, 2023, the NRC inspectors discussed the results of this inspection with Mr. Joe Quinn and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Louis J. McKown, II, Chief Reactor Projects Branch Division of Reactor Projects Docket Nos. 05000259, 05000260 and 05000296 License Nos. DPR-33, DPR-52 and DPR-68

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000259, 05000260 and 05000296

License Numbers:

DPR-33, DPR-52 and DPR-68

Report Numbers:

05000259/2022004, 05000260/2022004 and 05000296/2022004

Enterprise Identifier:

I-2022-004-0013

Licensee:

Tennessee Valley Authority

Facility:

Browns Ferry Nuclear Plant

Location:

Athens, Alabama

Inspection Dates:

October 01, 2022 to December 31, 2022

Inspectors:

B. Bowker, Reactor Inspector

P. Cooper, Senior Reactor Inspector

S. Downey, Senior Reactor Inspector

N. Karlovich, Resident Inspector

D. Lanyi, Senior Operations Engineer

K. Pfeil, Resident Inspector

M. Schwieg, Senior Reactor Inspector

J. Steward, Senior Resident Inspector

S. Temple, Resident Inspector

J. Vasquez, Construction Inspector

Approved By:

Louis J. McKown, II, Chief

Reactor Projects Branch 5

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Browns Ferry Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000259,05000260/20 21-001-01 LER 2021-001-01 for Browns Ferry Nuclear Plant,

Units 1 and 2, 480 Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications due to Failed Relay 71153 Closed

PLANT STATUS

Unit 1 began the inspection period in Mode 3 (Hot Shutdown) in support of a planned refueling outage (1R14). The licensee commenced unit startup on October 26, 2022 and returned to 100 percent (full) rated thermal power (RTP) on November 1, 2022. On November 3, 2022, operators down powered the unit to 38 percent RTP for emergent repairs to reactor recirculation loop B variable frequency drive (VFD). On November 4, 2022, operators returned the unit to RTP, where it remained throughout the inspection period.

Unit 2 began the inspection period at RTP. On November 11, 2022, reactor feed pump turbine (RFPT) B tripped which lowering reactor vessel water level resulted in an automatic reactor recirculation system runback to 75 percent. Operators maintained power at approximately 73 percent RTP during the corrective maintenance window. On November 15, 2022, Unit 2 was returned to full RTP and operated there until November 18, 2022, when power was lowered to 85 percent RTP for a control rod adjustment. On November 19, 2022, the unit was returned to full RTP. On November 26, 2022, power was lowered to 70 percent RTP for planned control rod exchange and surveillance testing and was returned to RTP later that day. On December 30, 2022, power was lowered to 74 percent RTP for a planned rod sequence exchange to all rods out configuration in preparation for coastdown to a planned refueling outage (2R22). On December 31, 2022, the unit was returned to full RTP where it operated at or near this level for the remainder of the inspection period.

Unit 3 began the inspection period at full RTP. On December 2, 2022, the unit was taken off-line to commence a planned forced outage (F311) to replace a defective fuel bundle as well as identify the source of increased floor drain leakage inside the drywell observed during the operating cycle. Unit startup commenced on December 10, 2022 and RTP was achieved on December 12, 2022. The unit remained at or near this level throughout the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending severe thunderstorms on November 29, 2022.

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated that flood protection barriers, mitigation plans, procedures, and equipment are consistent with the licensees design requirements and risk analysis assumptions for coping with external flooding on December 1, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 3 Core Spray (CS) Loop 2 while CS Loop 1 was under a planned flow test on November 3, 2022
(2) Unit 1 Reactor Core Isolation Cooling System while Unit 1 High Pressure Coolant Injection (HPCI) was removed from service for planned maintenance on the gland seal leak off piping on November 17, 2022
(3) Unit 3 Emergency Diesel Generator (EDG) 3C on December 4, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Area 8, 2B Electric Board Room including 4.16 KV Shutdown Board D, Unit 2 Control Bay 593' Elevation on October 2, 2022
(2) Fire Areas 01-04 and 01-03, Reactor Water Cleanup Heat Exchanger Room on elevation 593' on October 17, 2022
(3) Fire Area 02-03 and 02-04, Reactor Building Unit 2 Elevation 593' on October 21, 2022
(4) Fire Area 03-01, Reactor Building Unit 3 Elevation 519' and 541' NW, SW, NE, and SE quadrants on November 3, 2022
(5) Fire Area 26, Unit 1 Turbine Building elevation 617' on December 15, 2022

71111.08G - Inservice Inspection Activities (BWR)

BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01)

(1) The inspectors evaluated the boiling water reactor non-destructive examinations from October 3, 2022 to October 10, 2022:

Ultrasonic examination on the N-9 reactor vessel penetration weld

Visual examination on the RHR piping supports

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), "Requalification Requirements," of the NRC's "Operator's Licenses." During the week of December 5, 2022, the inspector performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, "Licensed Operator Requalification Program." These results were compared to the thresholds established in Section 3.03, "Requalification Examination Results," of IP 71111.11.

The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam completed on September 27, 2022.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Unit 1 Control Room during reactor startup including control rod withdrawal to achieve criticality following planned refueling outage (1R14) on October 26, 2022

The inspectors observed and evaluated licensed operator performance in the Unit 1 Control Room during reactor startup including control rod withdrawal and reactor mode switch manipulation to shift operating mode from MODE 2 to MODE 1 following planned refueling outage (1R14) on October 26, 2022

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification crew classroom training which reviewed the following topics as part of Cycle 2206, "Welcome to Requal", "Safeguards Event Reporting" and "FLEX Response Instructions" on November 29, 2022

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Unit 1 reactor recirculation pump 1B VFD cooling water line replacement per work order (WO) 123229093 on November 10, 2022
(2) Unit 3 fuel pool cooling and clean-up pump B motor replacement per WO 122484839 on December 14, 2022
(3) Common Unit Reactor Floor Crane Sheave Bearings failure and corrective maintenance per condition report (CR) 1821866 on December 15, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Observed emergent work on Unit 1 Turbine Control Valve No 2 per WO 123274163 on October 28, 2022
(2) Evaluated various activities during yellow (medium) site aggregate risk due to Unit 1 Reactor less than 90 percent RTP while maneuvering reactor power in accordance with 1-GOI-100-12, Power Maneuvering on November 1, 2022
(3) Unit 3 High Risk Evolution (Yellow Risk) during high decay heat, RPV Head removed and the reactor cavity drained in preparation for vessel flood up per GOI-100-3A, "Refueling Operations (Rx Vessel Disassembly and Floodup)", and 3-OI-2, "Condensate", on December 4, 2022
(4) Unit 3 Probabilistic (PRA) evaluation for using Technical Specification (TS) Limiting Condition for Operation (LCO) 3.0.4b to justify changing operating modes with TS 3.7.4 unmet going from MODE 4 to MODE 2 to MODE 1 on December 10, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (7 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Excessive four fill average boil-off rate for Containment Air Dilution (CAD) Tank B per CR 1792706 on October 5, 2022 (2)3-SR-3.1.7.3, Standby Liquid Control System Enriched Sodium Pentaborate (SPB)

Solution Concentration, Quantity Calculation and Anticipated Transient Without Scram (ATWS) Equivalency Calculation per CRs 1810303 and 1810362 on October 19, 2022

(3) As left maximum closing thrust exceeded the calculated allowable actuator thrust for the Unit 1 HPCI steam line inboard isolation valve, 1-FCV-073-0002 per CR 1808791 on November 2, 2022
(4) Emergency Equipment Chill Water (EECW) North Header Supply to northwest CS pump room cooler has packing leak per CR 1804496 on November 8, 2022
(5) Control Rod Drive Temperature Element at drive location 06-47 went from stable 115 degrees Fahrenheit (F) reading to over 700 degrees F per CR 1822164 on December 15, 2022
(6) Unit 3 EDG 3D received a Fast Start failure annunciator during surveillance testing per CR 1823305 on December 20, 2022
(7) C3 EECW pump and strainer unable to be rotated per CR 1804874 on December 30, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Unit 1 temporary modification of recirculation loop 'A' flow measurement instrumentation during outage U1R14 in October 2022
(2) Unit 1 permanent modification to document the HPCI Gland Seal Piping reroute and evaluate the added pipe supports for seismic qualification per design change package BFN-22-059 on November 25, 2022

Severe Accident Management Guidelines (SAMG) Update (IP Section 03.03) (1 Sample)

(1) The inspectors verified the site Severe Accident Management Guidelines were updated in accordance with the BWR generic severe accident technical guidelines and validated in accordance with NEI 14-01, Emergency Response Procedures and Guidelines for Beyond Design Basis Events and Severe Accidents, Revision 1.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Unit 1 HPCI Pump 150 psig test developed head and flowrate testing following overhaul preventive maintenance per WO 122585535 on October 26, 2022
(2) Unit 1 B reactor recirculation pump VFD A5 power cell replacement due to internal coolant leakage per WO 123279027 on November 8, 2022
(3) Unit 1 HPCI main and booster pump set developed head and flow rate testing following maintenance performed on gland seal leakoff lines for the auxiliary oil pump per WO 123261303 on November 18, 2022
(4) Unit 3 CS Pump A control transfer switch, 3-XSW-075-0005, testing after installation of a PK test block was added to the circuit per WO 123315808 on November 22, 2022
(5) Unit 1 Outer Equipment Access Airlock Doors following replacement of the limit switches for door 229B per WO 123355992 on December 19, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated various activities associated with a planned Unit 1 refueling outage from October 1 through October 27, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) Unit 1 drywell control air header isolation valves 1-CKV-32-336 and 1-CKV-32-915 and Containment Atmospheric Dilution primary containment isolation valves 1-SHV-84-686 and 1-FSV-84-49 local leak rate tests on October 18, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) A training drill scenario which included seismic activity, emergency medical response, loss of the B shutdown board, loss of feedwater, and main steam line valve isolation as well as degrading containment conditions requiring implementation of severe accident mitigation guidelines on November 30,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 (October 1, 2021 through September 30, 2022)
(2) Unit 2 (October 1, 2021 through September 30, 2022)
(3) Unit 3 (October 1, 2021 through September 30, 2022)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (3 Samples)

(1) Unit 1 (October 1, 2021 through September 30, 2022)
(2) Unit 2 (October 1, 2021 through September 30, 2022)
(3) Unit 3 (October 1, 2021 through September 30, 2022)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (3 Samples)

(1) Unit 1 (October 1, 2021 through September 30, 2022)
(2) Unit 2 (October 1, 2021 through September 30, 2022)
(3) Unit 3 (October 1, 2021 through September 30, 2022)

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Repairs and corrective actions associated with Unit 2 Reactor Feedwater Pump Turbine tripping on November 11, 2022 due to the Woodward 505 governor failure and a subsequent trip on November 14, 2022, due to a faulty time relay.
(2) Corrective actions and work orders associated with the setting of the Unit 2 CS pump room cooler 2B flow rate on July 15, 2022, after valve BFN-2-THV-067-0594 was replaced

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Followup (IP Section 03.01)

(1) The inspectors evaluated a high temperature condition in the Unit 3 Reactor Water Cleanup Heat Exchanger Room and licensees response on October 16, 2022

Event Report (IP Section 03.02) (1 Sample)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 2021-001-01 for Browns Ferry Nuclear Plant, Units 1 and 2, 480 Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications due to Failed Relay (ADAMS Accession No. ML22188A133). The inspectors reviewed the updated LER submittal on December 5, 2022. The previous LER submittal was reviewed in Inspection Report 05000259/2022001, 05000260/2022001, and 05000296/2022001 (ADAMS Accession No. ML21117A405). The inspection conclusions associated with this LER are documented in Inspection Report 05000259/2022001,

===05000260/2022001, and 05000296/2022001 (ADAMS Accession No. ML21117A405) under Inspection Results.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 71003 - Post-Approval Site Inspection for License Renewal Post-Approval Site Inspection for License Renewal===

(1) Carbon Steel/Raw Uncontrolled Water Monitoring Program

Motor Generator Oil Drain Header Check Valve (0-CKV-077-0545)

Motor Generator Oil Drain Header Check Valve (0-CKV-077-0618)

Off-Gas Condenser Drain Sump Pump B Discharge Check Valve (0-CKV-077-0708B)

Unit 1 Reactor Building Floor Drain Pump A Discharge Check Valve (1-CKV-077-0606)

Unit 1 Reactor Building Floor Drain Pump B Discharge Check Valve (1-CKV-077-0609)

Unit 1 Decontamination Drain Header Check Valve (1-CKV-077-0660)

Unit 1 Drywell Equipment Drain Sump Discharge Check Valve (1-CKV-077-0671)

Unit 1 Cleanup Backwash Transfer Discharge Line Check Valve (1-CKV-077-0929)

Unit 3 Sump Pump Discharge Check Valve (3-CKV-077-0670)

Unit 3 Drywell Equipment Drain Sump Discharge Check Valve (3-CKV-077-0671)

(2) One Time Inspection Program

Diesel Generator 0A (0-ENG-082-000A)

Diesel Generator 3B (3-ENG-082-003B)

Unit 1 Condensate Storage Tank (1-TNK-002-1462)

Unit 2 Condensate Storage Tank (2-TNK-002-1462)

Diesel Generator 3A Seven Day Oil Supply Tank (3-TNK-018-0061)

Diesel Generator 3D Seven Day Oil Supply Tank (3-TNK-018-0064)

High Pressure Fire Pump Diesel Fuel Oil Storage Tank (0-TNK-018-0803)

(3) Bus Inspection Program

4160 V non-segregated phase bus between USST 1A and Unit Board 1C

4160 V non-segregated phase bus between USST 1B and Unit Boards 1A and 1B

4160 V non-segregated phase bus between USST 2A and Unit Board 2C

4160 V non-segregated phase bus between USST 2B and Unit Boards 2A and 2B

4160 V non-segregated phase bus between USST 3A and Unit Board 3C

4160 V non-segregated phase bus between USST 3B and Unit Boards 3A and 3B

(4) Structures Monitoring Program and Water-Control Structures

Electrical Cable Tunnel from the Intake Pumping Station to the Powerhouse

Residual Heat Removal Service Water Tunnel

Diesel Generator Buildings

Transformer Yard

Reinforced Concrete Chimney

Intake Pumping Station

Gate Structure No. 2

Gate Structure No. 3

Intake Channel

Discharge Control Structure

North Bank of Cool Water Channel East of Gate Structure No. 2

South Dike of Cool Water Channel Between Gate Structure No.'s 2 and 3

(5) Inspection of Overhead Heavy Load and Light Load Handling Systems

Reactor Building Crane

Unit 1 RB Recirculating Pump Motor 24-Ton Monorail South

Unit 2 RB Recirculating Pump Motor 24-Ton Monorail North

3A RHR Heat Exchanger 12-Ton Monorail

(6) Inaccessible Medium Voltage Cables not Subject to EQ

RHRSW Pump D1 Supply

RHRSW Pump C2 Supply

RHRSW Pump A3 Supply

(7) ASME Section XI Subsection IWE

Unit 2 UT of drywell liner plate near the sand bed region

Unit 1 the steel containment shells and their integral attachments

Unit 2 containment hatches and airlocks

Unit 3 seals, gaskets, and moisture barriers

(8) Fatigue Monitoring Program

Work Order# 122070299 - Perform fatigue usage monitoring in accordance with 0-Tl-19 for Units 1, 2, and

INSPECTION RESULTS

No findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 26, 2023, the inspectors presented the integrated inspection results to Mr.

Joe Quinn and other members of the licensee staff.

On October 6, 2022, the inspectors presented the Exit meeting for the Unit 1 ISI inspection results to Manu Sivaraman, Site Vice President and other members of the licensee staff.

On December 8, 2022, the inspectors presented the Exit meeting for licensee renewal phase 4 inspection results to Manu Sivaraman, Site Vice President and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1644485

PERFORM REPAIRS ON 4KV BUS BETWEEN USST 1A

& 1B AND THEIR ASSOCIATED BOARDS

10/15/2020

Corrective Action

Documents

CRs (by number)

27663, 330419, 338557, 541116, 679174, 1759254,

1776693

21380

During review of UFSAR Changes to UFSAR Appendix

O.1.29 to support the License

Renewal Phase 4 NRC Inspection, it was identified that

the October 4, 2021 NRC

Submittal of UFSAR Amendment 29 did not include

UFSAR Change 29-01.

2/06/2022

21777

September 2019 FSAR Change 29-001; O.1.29 ASME

Section XI, Subsection IWE Program.

2/07/2022

21827

NRC License Renewal Phase IV observation 1A USST

Transformer 4KV

2/07/2022

21836

NRC License Renewal Phase IV observation 3A USST

4KV Buss Metal Enclosure heating indication light

2/07/2022

Corrective Action

Documents

Resulting from

Inspection

21838

NRC License Renewal Phase IV observation 3B USST

4KV Buss Inspection Cover missing bolt

2/07/2022

0-TI-609

Aging Management Program Basis Document Bus

Inspection Program

Procedures

EPI-0-242-BUS001

Main Transformer, Unit Station Service Transformer and

Associated Bus Work

119415889

BUSS INSP - CSST'A'

10/15/2022

119966703

INSPECTION & PREVENTIVE MAINTENANCE ON U-3

BUSES AS DEFINED IN EPI-0-242-BUS001

10/22/2020

71003

Work Orders

Work Orders (by

number)

111229336, 113261155, 113261159, 114718910,

115483482, 115483484, 115615996, 116239119,

117196191, 117576709, 118504376, 119186207

Calculations

MDQ0999920112

Prevention of Backflow

Rev 4

0-47E830-1-LR

License Renewal Flow Diagram Radwaste

Rev 4

Drawings

0-47E830-9-LR

License Renewal Flow Diagram

Rev 1

71111.01

Procedures

0-AOI-100-7

Severe Weather

Rev 49

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NPG-SPP-07.1.8

Severe Weather and Natural Disasters

Rev 2

1-47E813-1

Flow Diagram Reactor Core Isolation Cooling System

Rev 42

3-47E610-18-2

Mechanical Control Diagram Fuel Oil System

Rev 22

Drawings

3-47E814-1

Flow Diagram Core Spray System

Rev 35

1-OI-71

Reactor Core Isolation Cooling System

Rev 34

3-OI-75

Core Spray System

Rev 76

3-OI-82

Unit 3 Standby Diesel Generator System

Rev 157

71111.04

Procedures

3-OI-82/ATT-1C

Unit 3 Standby Diesel Generator 3C Valve Lineup

Checklist

Rev 99

FPR-Volume 2

Fire Protection Report Volume 2

Rev 73

Fire Plans

FPR-Volume 2

Fire Protection Report Volume 2

Rev 74

Miscellaneous

NFPA 805 Fire

Protection Report

Appendix F

Fire Area 03-01

Rev 3

3-OI-82/ATT-3C

Unit 3 Standby Diesel Generator 3C Electrical Lineup

Checklist

Rev 98

NPG-SPP-18.4.7

Control of Transient Combustibles

Rev 16

71111.05

Procedures

NPG-SPP-18.4.8

Control of Ignition Sources (Hot Work)

Rev 13

R-048

UT examination N9-NV 60deg

10/09/2022

R-048

UT examination N9-NV 20deg

10/09/2022

R-048

UT examination N9-NV 35deg

10/09/2022

R-048

UT examination N9-NV 45deg

10/09/2022

NDE Reports

VE-12-065

Ultrasonic examination of N9-NV reactor vessel

penetration

11/08/2012

N-UT-78

PDI Generic Procedure for the Manual Ultasonic

Examination of Reactor Pressure Vessel Welds

PDI-UT-11

Generic Procedure for the Ultasonic Examination of

Reactor Pressure Vessel Nozzle-to Shell Welds

D

71111.08G

Procedures

PDI-UT-6

Generic Procedure for the Ultasonic Examination of

Reactor Pressure Vessel Welds

I

OPL173.061

FLEX Requalification Training

Rev 2

OPL173R227

Welcome to Requal

Rev 56

71111.11Q

Miscellaneous

OPL175.011

NSDP-1 Safeguards Event Reporting Overview

Rev 0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1-GOI-100-1A

Unit Startup

Rev 71

1-OI-47

Turbine-Generator System

Rev 74

Procedures

1-SR-3.1.3.5(A)

Control Rod Coupling Integrity Check

Rev 15

Calibration

Records

BFN-22-00001

Investigation of Out of Tolerance M&TE for E36593,

Digital Micro ohmmeter

1/26/2022

1807103

11/10/2022

1813580

11/10/2022

CR 1730569

Corrective Action

Documents

CR 1822227,

1772591, 1444907,

22234

Drawings

3-47E855-1

Flow Diagram Fuel Pool Cooling System

Rev 26

2484848,

2484839

71111.12

Work Orders

WO 122583784,

2910385,

2910383

Corrective Action

Documents

1812648

10/27/2022

Engineering

Evaluations

BFN-3-22-105

Probabilistic (PRA) Evaluation Response for the

application of TS LCO 3.0.4b for TS 3.7.4 for BFN-3-

AHU-031-0104 inoperable

2/9/2022

3-GOI-100-3A

Refueling Operations (Rx Vessel Disassembly and

Floodup)

Rev 76

3-OI-2

Condensate

Rev 79

NPG-SPP-09.11.1

Equipment out of service managment

Rev 13

Procedures

NPG-SPP-09.11.2

Risk Assessment Methods for Technical Specifications

Rev 4

71111.13

Work Orders

23274163

10/27/2022

1792706

10/05/2022

1804496

1810303, 1810362

10/19/2022

Corrective Action

Documents

CR 1808791

71111.15

Engineering

Evaluations

MDQ107320020058

MOV 1-FCV-073-0002, Operator Requirements and

Capablities

Rev 5

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

3-SR-3.1.7.3

Standby Liquid Control System Enriched Sodium

Pentaborate (SPB) Solution Concentration, Quantity

Calculation, and ATWS Equivalency Calculation

Rev 55

Procedures

NPG-SPP-06.8

Leak Reduction Program

Rev 9

Calculations

EDQ2092900118

Setpoint and Scaling Calculations for Neutron Monitoring

System & Recirculation Flow Loops

Rev 39

Corrective Action

Documents

1803817

Drawings

1-47E610-68-1

Mechanical Control Diagram Reactor Recirculation

System

Rev 26

BFN-1-2202-068-004

Temporary Replacement of Recirculation Loop 1A Flow

Measurement

10/18/2022

Engineering

Changes

BFN-22-059

HPCI Gland Seal Piping Reroute

11/18/2022

BWROG SAG Vol V

Severe Accident Guidelines for Modes 1-4

Rev 4

BWROG SAG Vol VI

Severe Accident Guidelines for Refueling Conditions

Rev 4

BWROG TSG

BWR Owner's Group Technical Support Guidelines

Rev 1

FCR-TVA-2022-1816

Adds new pipe supports based on discovery of existing

flex hoses and documents as constructed piping

configuration

11/17/2022

Miscellaneous

TP21-1-008

Emergency Procedures Committee Generic Validation of

EPG/SAG Rev. 4 SAGs and Plant-Specific Validation of

SAMGS

Rev 0

1-SAMG-1

RPV and Primary Containment Control Modes 1-4

Rev 4

1-SAMG-1RF

RPV and Primary Containment Level Control Mode 5

Rev 0

1-SAMG-2

RPV, Containment, and Radioactivity Release Control

Modes 1-4

Rev 7

1-SAMG-2RF

RPV, Containment, and Radioactivity Control Mode 5

Rev 0

2-SAMG-1

RPV and Primary Containment Control Modes 1-4

Rev 11

2-SAMG-1RF

RPV and Primary Containment Level Control Mode 5

Rev 0

2-SAMG-2

RPV, Containment, and Radioactivity Release Control

Modes 1-4

Rev 11

2-SAMG-2RF

RPV, Containment, and Radioactivity Control Mode 5

Rev 0

3-SAMG-1

RPV and Primary Containment Control Modes 1-4

Rev 9

71111.18

Procedures

3-SAMG-1RF

RPV and Primary Containment Level Control Mode 5

Rev 0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

3-SAMG-2

RPV, Containment, and Radioactivity Release Control

Modes 1-4

Rev 13

3-SAMG-2RF

RPV, Containment, and Radioactivity Control Mode 5

Rev 0

NPG-SPP-18.3.1

Severe Accident Management Guideline Program

Administration

Rev 8

Work Orders

23254158

11/25/2022

Procedures

1-SR-3.5.1.8

HPCI Main and Booster Pump Set Developed Head and

Flow Rate Test at 150 psig Reactor Pressure

Rev 17

2585535,

21882390

10/26/2022

71111.19

Work Orders

WO 123315808,

23279027, and

23261303

Engineering

Evaluations

EWR21NSSS069238

Evaluate the requested changes to 1/2/3-OI-78 for RPV

hardening given TSTF-542 and 582 changes to BFN

Technical Specification requirements

10/05/2022

1-OI-74

Residual Heat Removal System

Rev 122

1-OI-78

Fuel Pool Cooling and Cleanup System

Rev 71

71111.20

Procedures

1-POI-78

Reactor Water Letdown During Refueling Outages

Rev 10

Procedures

1-SI-4.7.A.2.g-3/32b

Primary Containment Local Leak Rate Test Control Air:

Penetration X-22

Rev 8

71111.22

Work Orders

WO 122108522

71114.06

Miscellaneous

22 BFN November Training Drill Scenario Guide

11/30/2022

Corrective Action

Documents

CR 1798942

BFN Unit 1, 2, and 3

1E01 data by Month

Performance indicator Data for Unit 1, 2, and 3 for 1E01

11/28/2022

NEI 99-02

Regulatory Assessment Performance Indicator Guideline

Rev 7

71151

Miscellaneous

U1, U2, U3 2022Q3

ROP data and ROP summary documents

11/01/2022

1816156, 1816590,

1816796, 1816240

Corrective Action

Documents

CR 1804818,

1789922

71152A

Work Orders

WO 123042561

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

1809667

10/17/2022

71153

Work Orders

2933661

10/17/2022