IR 05000259/2022003

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Browns Perry Nuclear Plant - Integrated Inspection Report 05000259/2022003, 05000260/2022003 and 05000296/2022003
ML22312A497
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 11/09/2022
From: Wesley Deschaine
NRC/RGN-II/DRP/RPB5
To: Jim Barstow
Tennessee Valley Authority
References
IR 2022003
Download: ML22312A497 (17)


Text

SUBJECT:

BROWNS FERRY NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000259/2022003, 05000260/2022003 AND 05000296/2022003

Dear Mr. Barstow:

On September 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Browns Ferry Nuclear Plant. On November 3, 2022, the NRC inspectors discussed the results of this inspection with Mr. Manu Sivaraman and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Wesley D. Deschaine, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Nos. 05000259, 05000260 and 05000296 License Nos. DPR-33, DPR-52, and DPR-68

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000259, 05000260 and 05000296

License Numbers:

DPR-33, DPR-52 and DPR-68

Report Numbers:

05000259/2022003, 05000260/2022003 and 05000296/2022003

Enterprise Identifier:

I-2022-003-0013

Licensee:

Tennessee Valley Authority

Facility:

Browns Ferry Nuclear Plant

Location:

Athens, Alabama

Inspection Dates:

July 01, 2022 to September 30, 2022

Inspectors:

N. Karlovich, Resident Inspector

M. Kirk, Resident Inspector

M. Meeks, Senior Operations Engineer

N. Peterka, Fuel Facility Inspector

K. Pfeil, Resident Inspector

J. Steward, Senior Resident Inspector

J. Viera, Senior Operations Engineer

Approved By:

Wesley D. Deschaine, Chief

Reactor Projects Branch 5

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Browns Ferry Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000259/2022003-01 Browns Ferry Unit 1 High Pressure Coolant Injection (HPCI) Inoperable on July 12, 2022 71152S Open

PLANT STATUS

Unit 1 began the inspection period in Mode 1, 100 percent (full) rated thermal power (RTP). On July 6, 2022, the Unit down powered to 77 percent RTP in order to comply with the State of Alabama National Pollutant Discharge Elimination (NPDES) Permit which limits the temperature of heated effluent from the plant such that the 24-hour average downstream plant-induced water temperature should not exceed 90 degrees F. On July 7, 2022, downstream plant-induced water temperature was maintained such that Unit 1 returned to 100 percent RTP. On July 8, 2022, Unit 1 down powered to 51 percent RTP in order to comply with NPDES 24-hour average downstream plant-induced water temperature requirements and returned to full RTP on July 10, 2022. On July 11, 2022, Unit 1 down powered to 70 percent RTP for a control rod pattern adjustment and returned to full RTP on July 12, 2022. On August 22, 2022, Unit 1 commenced coast down in power in anticipation of a planned refueling outage (1R14). On September 1, 2022, reactor recirculation pump 1A tripped due to multiple power cells being bypassed on the 1A variable frequency drive (VFD) which lowered power to 38 percent RTP. On September 5, 2022, following repairs to the VFD power was raised to 95 percent RTP. Unit 1 continued to coast down in power until reactor recirculation pump 1B tripped due to multiple power cells being bypassed on the 1B VFD on September 28, 2022, which lowered power from 83 percent RTP to approximately 40 percent RTP. Unit 1 remained at 40 percent power until the unit was shutdown on September 30, 2022, at 2100 for the 1R14 refueling outage, where it remained through the end of the inspection period.

Unit 2 began the inspection period at full RTP. On September 15, 2022, Unit 2 performed a planned down power to 62 percent RTP for testing of the turbine control valve and then returned to full RTP where it remained through the end of the inspection period.

Unit 3 began the inspection period at full RTP. On July 8, 2022, Unit 3 down powered to 78 percent RTP in order to comply with NPDES 24-hour average downstream plant-induced water temperature requirements and returned to full RTP on July 9, 2022. On August 26, 2022, Unit 3 down powered to 65 percent RTP for a planned control rod pattern adjustment. On August 28, 2022, Unit 3 returned to full RTP. On September 6, 2022, Unit 3 down powered to 63 percent RTP for power suppression testing due to indications of damaged fuel. On September 10, 2022, Unit 3 returned to full RTP. On September 23, 2022, Unit 3 down powered to 70 percent for a planned control rod sequence exchange and returned to full RTP on September 24, 2022, where it remained through the end of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 Core Spray Loop 1 while Core Spray Loop 2 was under planned maintenance on July 13, 2022
(2) Unit 2 Residual Heat Removal System (RHR) Loop 2 on September 09, 2022
(3) Unit 0 "A" Control Bay Chiller pump and Chiller while B Chiller was under planned maintenance on September 15, 2022

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1, 2 and 3 Containment Atmosphere and Dilution (CAD) system on August 17, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Area 5, Electric board room 1A on August 9, 2022
(2) Fire Area 18, Unit 2 Battery and battery board room on August 9, 2022
(3) Fire Area 16, Units 2 and 3 Cable Spreading room B on September 16, 2022

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 3 Emergency Diesel Generator (EDG) Building on June 21-24, 2022, and August 10, 2022

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

The inspectors reviewed the facility operating history and associated documents in preparation for this inspection. During the week of September 12, 2022, the inspectors reviewed documentation, interviewed licensee personnel, and observed the administration of operating tests associated with the licensees operator requalification program. Each of the activities performed by the inspectors was done to assess the effectiveness of the facility licensee in implementing requalification requirements identified in 10 CFR Part 55, Operators Licenses. The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program. The inspectors also evaluated the licensees simulation facility for adequacy for use in operator licensing examinations using ANSI/ANS-3.5-1985, American National Standard for Nuclear Power Plant Simulators for use in Operator Training and Examination. The inspectors observed three crews during the performance of the operating tests. Documentation reviewed included written examinations, Job Performance Measures (JPMs), simulator scenarios, licensee procedures, on-shift records, simulator modification request records, simulator performance test records, operator feedback records, licensed operator qualification records, remediation plans, watchstanding records, and medical records. The records were inspected using the criteria listed in IP 71111.11. Documents reviewed during the inspection are documented in the List of Documents Reviewed.

(1) Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examination administered in 2021.

Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.

Administration of an Annual Requalification Operating Test The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during the following evolutions:

Unit 1 downpower due to river temperature on July 6, 2022

Unit 1 removal of extraction steam from feedwater heaters 1A1, 1B1 and 1C1 to implement final feedwater temperature reduction on August 20, 2022

Unit 3 downpower to 70 percent RTP and removal of 3A Reactor Feed Pump Turbine from service on August 26, 2022

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated two separate licensed operator requalification training sessions which included a control rod drift, loss of Emergency Equipment Cooling Water (EECW), Safety Relief Valve (SRV) lift, Electro Hydraulic Control (EHC) system leak, high power Anticipatory Transient Without Scram (ATWS), high suppression chamber pressure caused by SRV tailpipe break on the Unit 2 simulator on August 15, 2022, which required the crew to enter various abnormal operating instructions (AOI), emergency operating instructions (EOI) and emergency plan Implementing procedures (EPIP) to control the plant and appropriately classify the emergency.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) RHR 1A Heat Exchanger Outlet Valve, 1-FCV-23-34 loss if indication during closure stroke from the main control room and subsequent actuator replacement maintenance activity on August 18, 2022
(2) Maintenance Rule Periodic Evaluation, 50.65(a)(3) for January 2020 through December 2021 completed on September 21, 2022
(3) Diesel Exhaust Board 3EB Room Exhaust Fan found tripped, work order 123060605 written and documented maintenance rule functional failure on September 28, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Evaluated risk of various Unit 1, Unit 3 and common protected equipment while EDG A removed from service during planned maintenance on August 2, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 2, System 2 Minimum Flow Isolation Valve Operator, 2-MVOP-075-0037 as found close stem factor exceeded acceptance criteria on September 22, 2022
(2) Unit 1, RHR Loop 1 LPCI outboard injection valve,1-FCV-074-0052, having a worn bearing found in the gear train on September 23, 2022
(3) Unit 1, 2, and 3 nitrogen storage tank A fill line safety valve, 0-RFV-084-0503, experiencing excessive leakage during relief valve testing on September 16, 2022
(4) Unit 1 reactor building equipment access inner door leak failure of 0-TI-408 per CR

===1700900 on September 28, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01)===

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Unit 1, HPCI turbine control valve, 1-FCV-73-19, after replacement on the electronic governor (EG-R) actuator on July 16, 2022
(2) Units 1 and 2, A diesel generator (DG) following generator replacement on August 4, 2022
(3) Unit 0, a battery charger after replacement of the Shutdown Board D 250 V DC Battery Charger on September 22, 2022
(4) Unit 0, breaker 0-BKR-031-2201A, for the 480V Supply for control bay chilled water pump B, after the breaker was returned from cleaning on September 22, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (1 Sample)

(1) Unit 3 Control Rod Coupling Integrity Check during power suppression testing on September 08, 2022

Inservice Testing (IP Section 03.01) (2 Samples)

(1) Unit 0 (Common) Residual Heat Removal Service Water (RHRSW) C3 IST Group A Quarterly Pump Test on August 31, 2022
(2) Unit 0 (Common) Residual Heat Removal Service Water (RHRSW) Pump C1 IST Group A Quarterly Pump Test on September 26, 2022

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) Unit 3, Drywell Floor Drain Leakage Rate rise documented under CR 1795731 which triggered entry on August 9, 2022, into Action Level 3 of Inspection Manual Chapter 2515, Appendix D, Attachment 1

FLEX Testing (IP Section 03.02) (1 Sample)

(1) Flex Equipment Storage Building (FESB) Inspection and Maintenance on August 30, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) The inspectors reviewed and evaluated the emergency response organization drill response during a Unit 2 shutdown Mode 4 scenario that required the facilities to correctly classify the event and notify the required outside organizations within the required timeframes on July 27,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05)===

(1) Unit 1 (July 1, 2021 - June 30, 2022)
(2) Unit 2 (July 1, 2021 - June 30, 2022)
(3) Unit 3 (July 1, 2021 - June 30, 2022)

MS09: Residual Heat Removal Systems (IP Section 02.08) (3 Samples)

(1) Unit 1 (July 1, 2021 - June 30, 2022)
(2) Unit 2 (July 1, 2021 - June 30, 2022)
(3) Unit 3 (July 1, 2021 - June 30, 2022)

MS10: Cooling Water Support Systems (IP Section 02.09) (3 Samples)

(1) Unit 1 (July 1, 2021 - June 30, 2022)
(2) Unit 2 (July 1, 2021 - June 30, 2022)
(3) Unit 3 (July 1, 2021 - June 30, 2022)

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Corrective actions associated with relay contacts for the Unit 3 3C RHR pump 4kV shutdown board breaker not responding as expected while performing preventative maintenance on August 26, 2022
(2) Repairs and corrective actions associated with Unit 3 Drywell Pressure High indicator reading high and indicating trip condition due to water intrusion in the pressure transmitter on June 22, 2022

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in increasing trend in moisture content in the Unit 1 HPCI turbine oil samples that might be indicative of a more significant safety issue on September 30, 2022

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Followup (IP Section 03.01)

(1) The inspectors evaluated unplanned inoperability of Unit 1 HPCI due to the failure of the turbine control valve to open during a surveillance and licensees response on July 12,

INSPECTION RESULTS

Unresolved Item (Open)

Browns Ferry Unit 1 High Pressure Coolant Injection (HPCI) Inoperable on July 12, 2022 URI 05000259/2022003-01 71152S

Description:

On July 12, 2022, during the performance of the Browns Ferry (BF) Unit 1 HPCI quarterly flow test, operators started the auxiliary oil pump, but the HPCI governor valve failed to open. The governor valve controls flow of steam to the HPCI pump turbine. With the governor valve closed the HPCI system cannot perform its safety function. The licensee subsequently declared Unit 1 HPCI inoperable at 0954 central time. The Automatic Depressurization System (ADS) and Reactor Core Isolation Cooling (RCIC) systems remained operable. This condition placed the unit into Technical Specification action statement LCO 3.5.1.C, which provides the licensee 14 days to restore HPCI to operation. Following replacement of the EGR (Electronic Governor Remote), remote servo and post maintenance testing, HPCI was restored to operable at 0915 on July 15, 2022.

The licensee reported the event to the NRC on July 12, 2022, under event number 55992 as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v) and submitted a written report as Licensee Event Report (LER) 50-259/2022-002-00, HPCI Inoperable Due to Corroded Actuator on September 12, 2022. The licensee completed a Level 2 Evaluation Report titled, Unit 1 HPCI Turbine Control Valve Failed to Open documented under Condition Report (CR) 1789217 on August 17, 2022. HPCI Failure Analysis of the Woodward EGR Actuator, Rev.0 was performed by third party vendor Engine Systems Inc., on August 17, 2022. Revision 1 to the Failure Analysis of the Woodward EGR Actuator was issued on October 3, 2022. The licensee approved a Management Review Committee (MRC) endorsed version of a revision to the Level 2 Evaluation Report titled, Unit 1 HPCI Turbine Control Valve Failed to Open on October 17, 2022. Issuance of revision 2 to the Failure Analysis of the Woodward EGR Actuator is pending.

An unresolved item (URI) is opened to review the MRC endorsed version of the Level 2 Evaluation and the pending revision 2 of the failure analysis of the Woodward EGR Actuator to determine if there is a performance deficiency and when BF Unit 1 HPCI was inoperable.

Planned Closure Actions: NRC subject matter experts (SMEs) will review the licensees evaluation of the issue and will document the results in the BF fourth quarter integrated inspection report.

Licensee Actions: On July 21, 2022, scope add 1372 and WO 114560684, "Unit 1 HPCI Gland Seal Leak-off lines need to be routed downward, were added to the outage scope for the 1R14 refueling outage commencing October 1, 2022.

Corrective Action References: CRs 1552443, 1729940, 1789217, 1790363 and WO

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On November 3, 2022, the inspectors presented the integrated inspection results to Mr.

Manu Sivaraman and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

0-47E866-9

Flow Diagram Chilled Water Circulating Pumps

Rev 14

1-47E862-1

Units 1 and 0 Flow Diagram Containment Atmosphere

Dilution System

Rev 27

1-OI-84-ATT-2A

Containment Atmosphere Dilution System Panel Lineup

Checklist

Rev 8

2-47E811-1

Flow Diagram Residual Heat Removal System

Rev 77

2-47E814-1

Flow Diagram Core Spray System

Rev 56

Drawings

3-47E862-1

Unit 3 Flow Diagram Containment Atmosphere Dilution

System

Rev 32

0-OI-31

Control Bay and Off-Gas Treatment Building Air

Conditioning System

Rev 172

0-OI-31/ATT-1

Valve Lineup Checklist

Rev 137

0-OI-31/ATT-2

Panel Lineup Checklist

Rev 136

0-OI-31/ATT-3

Electrical Lineup Checklist

Rev 137

0-OI-31/ATT-4

Instrument Inspection Checklist

Rev 137

1-OI-84/ATT-1A

Containment Atmosphere Dilution System Valve Lineup

Checklist

Rev 10

2-OI-75

Core Spray System

Rev 120

2-OI-75/ATT-1

Core Spray System Valve Lineup Checklist

Rev 106

2-OI-75/ATT-2

Panel Lineup Checklist Unit 2

Rev 107

2-OI-75/ATT-3

Cores Spray System Electrical Lineup Checklist

Rev 106

2-OI-75/ATT-4

Core Spray System Instrument Inspection Checklist

Rev 105

2-OI-84/ATT-1

Containment Atmosphere Dilution System Valve Lineup

Checklist

Rev 51

3-OI-84/ATT-1A

Containment Atmosphere Dilution System Valve Lineup

Checklist

Rev 31

71111.04

Procedures

3-OI-84/ATT-2A

Containment Atmosphere Dilution System Panel Lineup

Checklist

Rev 29

0-47E216-106

Ignition Source Drawings Plan El. 606.0 and 621.25

Rev 3

Drawings

0-47E216-70

NFPA 805 Fire Areas Plan El. 617.0 and 621.25

Rev 1

71111.05

Fire Plans

NFPA 805 Fire Protection Report - Appendix F, Fire

Safety Analysis

Rev 0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

FPR-Volume 2

Fire Protection Report Volume 2

Rev 73

NFPA 805 Protection

Report

Appendix F Fire Area 16

Rev 5

MDQ00004020110008

Flow Capacity of the Diesel Generator Building

Emergency Drain Piping

Rev 1

Calculations

NDN00099920070031

BFN Probabilistic Risk Assessment - Internal Flooding

Analysis

Rev 3

Drawings

0-47E851-4

Flow Diagram Drainage

Rev 18

0-OI-40

Station Drainage System

Rev 37

71111.06

Procedures

3-ARP-9-7C

Panel 9-7 3-XA-55-7C

Corrective Action

Documents

Condition Reports

28394; 1738904; 1759998; 1627098; 1683693;

1692069; 1694927

JPM 0AREP20APTC

Hazards - Hostile Action within the Protected Area (HS1)

without Vaporstream

Rev 0

JPM 0AREP22APTC

HAZARDS - HOSTILE ACTION within the OWNER

CONTROLLED AREA or airborne attack threat within 30

minutes - without Vaporstream

Rev 0

JPM 1IPAOI06AP

Actions outside Control Room to attempt to close Unit 1

MSRV 1-18 per 1-AOI-1-1

Rev 0

JPM 1IPEO108

EOI Appendix 16L - Bypassing High Temperature

Isolation

Rev 1

JPM 1IPFSS38

Perform 1-FSS-16.2, Attachment 10, Section 2, Step C

to align Panel 25-31 for RCIC Operation at the Backup

Control Panel

Rev 0

JPM 2IPEOI06

EOI Appendix 16H - Bypassing RCIC High RPV Water

Level Shutdown Interlocks

Rev 7

JPM 2SAOI10AP

Respond to Single Recirc Pump Trip in Mode 1

Rev 3

JPM 2SEOI20

Align Shutdown Cooling from Unit 3 in accordance with

2-EOI Appendix 17E

Rev 0

JPM 3IPFSS20

Align 4KV Shutdown Board 3EA to Diesel Generator 3A

per 3-FSS-16-2, Attachment 6, Section 3.0

Rev 0

JPM 3SEOI22AP

3-EOI Appendix 17F, RHR Fails, use Loop II Core Spray

Rev 0

Medical Records

Medical Records reviewed for twelve licensed operators

71111.11B

Miscellaneous

Remediation Records

Five (5) Remedial Training Records (Individual and

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Crews) from 2-year Training Cycle

SEG# LOR-EXAM-26

Simulator Scenario LOR-EXAM-26

Rev #07

SEG# LOR-EXAM-77

Simulator Scenario LOR-EXAM-77

Rev #3

SEG# LOR-EXAM-

78A

Simulator Scenario LOR-EXAM-78A

Rev #0

SEG# LOR-EXAM-84

Simulator Scenario LOR-EXAM-84

Rev #00

Simulator Testing

Steady State Test, 74%, 11-29-2021; Steady State Test,

50%, 7-11-2022; Malfunction Test, FW30, 7-7-2022;

Malfunction Test, RD06, 7-10-2022; Malfunction Test,

TC01, 7-10-2022; Transient Test, 2021 #2, 11-2-2021;

Transient Test, 2021 #5, 11-2-2021; Transient Test,

22 #3, 6-27-2022; Transient Test, 2022 #7, 6-2-2022;

Transient Test, 2022 #8, 6-2-2022

Written Examination

21 NRC Biennial Examinations, RO and SRO

Examination 3

Miscellaneous

OPL1755494

Control Rod Drift/Loss of EECW/SRV Lift/EHC

Leak/ATWS EOI-1A/ High SC Pressure/EOI-2

Rev 0

1-GOI-100-12

Power Maneuvering

Rev 20

71111.11Q

Procedures

1-OI-6

Feedwater Heating and Misc Drains System

Rev 44

1794453

08/18/2022

Corrective Action

Documents

1794821, 1791930

09/28/2022

Self-

Assessments

R40 220224 179

Maintenance Rule 13th Periodic Report January 2020 to

December 2021

Rev 0

23060605

09/28/2022

71111.12

Work Orders

23091734

08/18/2022

Calculations

MDQ2075910144

Rev 6

CR 1222334827

Corrective Action

Documents

CR 1790852, 1711939

Operability

Evaluations

CR 1789337

09/22/2022

0-TI-408

Equipment Air Lock Door Seal Pressure Decay Test

Rev 11

NEDP-22

Operability Determinations and Functional Evaluations

Rev 23

71111.15

Procedures

OPDP-8

Operability Determination Process and Limiting

Conditions for Operation Tracking

Rev 29

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2245070

09/22/2022

Work Orders

WO 119853968,

21509559

1-47E812-1

Flow Diagram High Pressure Coolant Injection System

Rev 48

Drawings

1-47E812-2

Flow Diagram HPCI Oil System

Rev 5

Miscellaneous

BFN-VTD-W290-0030

Installation and Operation of Woodward EG-3C AND

EG-R Actuators

Rev 1

1-SR-3.5.1.7

HPCI Main and Booster Pump Set Developed Head and

Flow Rate Test at Rated Reactor Pressure

Rev 45

MCI-0-082-ENG014

Standby Diesel Engine Generator Removal and

Reinstallation

Rev 22

Procedures

MPI-0-073-TRB001

High Pressure Coolant Injection (HPCI) Turbine

Preventative Maintenance

Rev 58

WO 122110966,

2405721

71111.19

Work Orders

WO 122190143,

23038729,

23038489,

2196374

1-GOI-100-12

Power Maneuvering

Rev 20

1-GOI-100-12A

Unit Shutdown from Power Operation to Cold Shutdown

and Reductions in Power During Power Operations

Rev 38

71111.20

Procedures

1-OI-69

Reactor Water Cleanup System

Rev 86

79847

Preventive Maintenance Job Plan

Rev 2

Miscellaneous

ODMI

Operational Decision Making Issue Evaluation

Document on increasing Unit 3 Drywell Unidentified

Leakage

08/19/2022

0-SI-4.5.C.1(C1)

RHRSW Pump C1 IST Group A Quarterly Pump Test

Rev 12

Procedures

0-SI-4.5.C.1(C3)

RHRSW Pump C3 IST Group A Quarterly Pump Test

Rev 19

71111.22

Work Orders

2344501

08/30/2022

R40210928088

Unit 2 MSPI Basis Document

Rev 20

R40210928089

Unit 3 MSPI Basis Document

Rev 20

71151

Engineering

Evaluations

R4021098087

Unit 1 MSPI Basis Document

Rev 21

71152A

Corrective Action

CR 1785291,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1801867, 1785140

Documents

CR 1798886, 1799518

WO 122163858

Work Orders

WO 123183883,

23001232

Corrective Action

Documents

2443, 1729940,

1789217 and 1790363

10/17/2022

Miscellaneous

1372

Scope add

10/17/2022

71152S

Work Orders

114560684

10/17/2022