ML090350417

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Letter to Naslund, Amerenue from Smith, NRC, Callaway Plant NRC Problem Identification and Resolution Inspection Report 05000483-08-006
ML090350417
Person / Time
Site: Callaway Ameren icon.png
Issue date: 04/21/2008
From: Laura Smith
NRC/RGN-IV/DRS/EB-2
To: Naslund C
AmerenUE
References
FOIA/PA-2009-0042, RIV-2007-A-0130 IR-08-006
Download: ML090350417 (38)


See also: IR 05000483/2008006

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

611 RYAN PLAZA DRIVE, SUITE 400

ARLINGTON, TEXAS 76011-4005

April 21, 2008

Charles D. Naslund, Senior Vice

President and Chief Nuclear Officer

AmerenUE

P.O. Box 620

Fulton, MO 65251

SUBJECT: CALLAWAY PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION

INSPECTION REPORT 05000483/2008006

Dear Mr. Naslund:

On March 14, 2008, the U. S. Nuclear Regulatory Commission completed a team inspection at

your Callaway Plant. The enclosed report documents the inspection findings, which the team

discussed on March 14, 2008, with Mr. A. Heflin, Vice President - Nuclear, and other members of

your staff during-the exit meeting.

The team examined activities conducted under your license as they relate to the identification and

resolution of problems, compliance with the Commission's rules and regulations, and the

conditions of your operating license. Within these areas, the inspection involved examination of

selected procedures and representative records, observations of activities, and interviews with

personnel. The team reviewed 246 Callaway Action Requests, associated root and apparent

cause evaluations, and other supporting documents. The team reviewed an additional

124 Callaway Action Requests related to specific areas - essential service water, component

cooling water, 480 Vac auxiliary contacts, and safety conscious work environment. The team

reviewed cross-cutting aspects of NRC findings and interviewed personnel regarding the condition

of your safety conscious work environment at.the Callaway Plant.

Based on the sample selected for review, the team concluded that your staff continued to have

challenges in the area of prioritization and evaluation, which need additional attention. The team

also noted that performance related to problem identification and resolution had improved. The

team determined that you're your staff had used the self-assessment process and quality

assurance organization to improve site performance. The team determined the improvement

resulted from corrective action process improvements implemented in January 2007, and

management oversight process changes implemented following receipt of substantive

cross-cutting issue'in problem identification and resolution.

Because of the increased number of allegations at your facility in Calendar Year 2007, especially _

the discrimination concerns, the team interviewed a large number of personnel related to the /

safety conscious work environment at the Callaway Plant. In addition, because of the nature of

the concerns expressed in the allegations, the team asked additional questions to gain insights

into the safety conscious work environment at your facility. The team documented the nature of

the concerns and the scope of the evaluations in Attachment 3. The team determined that not all

individuals were comfortable using all of the methods available to them for reporting concerns;

however, all personnel interviewed stated that they would have used at least one of the methods

AmerenUE -2-

available for reporting a safety concern. The team determined that our review results remained

consistent with other safety culture surveys that you had completed within the last year. The team

determined that some general culture and work environment issues continued to be present that

were outside NRC regulatory jurisdiction, which if not addressed could potentially affect the safety

conscious work environment at the Callaway Plant.

The team identified one finding for failure to determine whether you had a non-conservative

technical specification surveillance requirement. The team attributed this to improper processing

of operating experience. This finding violated NRC requirements. However, because of the

finding had very low safety significance and because the finding had been entered into your

corrective action program, the NRC is treating this findings as a noncited violation, in accordance

with Section VI.A.1 of the NRC's Enforcement Policy. In addition, one licensee-identified violation

of very low safety significance is listed in this report. If you contest the violations or the

significance of the violations, you should provide a response within 30 days of the date of this

inspection report. Include the basis for your denial, to the U. S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional

Administrator, U. S. Nuclear Regulatory Commission, Region IV,611 Ryan Plaza Drive, Suite 400,

Arlington, Texas, 76011; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Callaway

Plant.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document Room

or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS).

ADAMS is accessible from the NRC web site at http://www.nrc.qov/readinq-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

IRA/

Linda J. Smith, Chief

Engineering Branch 2

Division of Reactor Safety

Docket: 50-483

License: NPF-30

Enclosure:

John O'Neill, Esq.

Pillsbury Winthrop Shaw Pittman LLP

2300 N. Street, N.W.

Washington, DC 20037

Scott A. Maglio, Assistant Manager

Regulatory Affairs

AmerenUE

P.O. Box 620

Fulton, MO 65251

AmerenUE -3-

Missouri Public Service Commission

Governor's Office Building

200 Madison Street

P.O. Box 360

Jefferson City, MO 65102-0360

H. Floyd Gilzow

Deputy Director for Policy

Missouri Department of Natural Resources

P. 0. Box 176

Jefferson City, MO 65102-0176

Rick A. Muench, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Kathleen Smith, Executive Director and

Kay Drey, Representative

Board of Directors Missouri Coalition

for the Environment

6267 Delmar Boulevard, Suite 2E

St. Louis City, MO 63130

Lee Fritz, Presiding Commissioner

Callaway County Courthouse

10 East Fifth Street

Fulton, MO 65251

.Les H, Kanuckel, Manager

Quality Assurance

AmerenUE

P.O. Box 620

Fulton, MO 65251

Director, Missouri State Emergency

Management Agency

P.O. Box 116

Jefferson City, MO 65102-0116

AmerenUE -4-

Scott Clardy, Director

Section for Environmental Public Health

Missouri Department of Health and

Senior Services

P.O. Box 570

Jefferson City, MO 65102-0570

Luke H. Graessle, Manager

Regulatory Affairs

AmerenUE

P.O. Box 620

Fulton, MO 65251

Thomas B. Elwood, Supervising Engineer

Regulatory Affairs and Licensing

AmerenUE

P.O. Box 620

Fulton, MO 65251

Certrec Corporation

4200 South Hulen, Suite 422

Fort Worth, TX 76109

Keith G. Henke, Planner III

Division of Community and Public Health

Office of Emergency Coordination

Missouri Department of Health and

Senior Services

930 Wildwood,

P.O. Box 570

Jefferson City, MO 65102

Technical Services Branch Chief

FEMA Region VII

2323 Grand Boulevard, Suite 900

Kansas City, MO 64108-2670

Ronald L. McCabe, Chief

Technological Hazards Branch

National Preparedness Division

DHS/FEMA

9221 Ward Parkway

Suite 300

Kansas City, MO 64114-3372

AmerenUE -5-

Electronic distribution by RIV:

Regional Administrator (EEC)

DRP Director (DDC)

DRS Director (RJC1)

DRS Deputy Director (TWP)

Senior Resident Inspector (DMD)

Branch Chief, DRP/B (VGG)

Senior Project Engineer, DRP/B (RWD)

Team Leader, DRP/TSS (CJP)

RITS Coordinator (MSH3)

DRS STA (DAP)

JTAdams, OEDO RIV Coordinator (JTA)

ROPreports

CWY Site Secretary (DVY)

SUNSI Review Completed: GAP ADAMS: 4 Yes Initials: GAP

4 Publicly Available 4 Non-Sensitive

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OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

ENCLOSURE

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-483

License: NPF-30

Report

05000483/2008006

Number:

Licensee: AmerenUE

Facility: Callaway Plant

Junction Highway CC and Highway 0

Location:

Fulton, Missouri

Dates: February 11 - 15, and March 10 - 14, 2008

Team Leader: G. Pick, Senior Reactor Inspector, Engineering Branch 2

Inspectors: R. Deese, Senior Project Engineer, Branch B, Division of Reactor Projects

J. Groom, Resident Inspector, Callaway Plant

S. Alferink, Reactor Inspector, Engineering Branch 2

P. Goldberg, Reactor Inspector, Engineering Branch 2

E. Uribe, Reactor Inspector, Engineering Branch 2

Approved By: Linda Smith, Chief

Engineering Branch 2

Division of Reactor Safety

- 1- Enclosure

SUMMARY OF ISSUES

IR 05000483/2008006; 2/11/2008 - 3/14/2008; Callaway Plant; Biennial inspection of the

identification and resolution of problems

One senior reactor inspector, one senior project engineer, three reactor inspectors, and a resident

inspector conducted the inspection. The team identified one noncited violation during this inspection.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, "Significance Determination Process." Findings for which the

Significance Determination Process does not apply may be Green or be assigned a severity level

after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process,"

Revision 4, dated December 2006.

Identification and Resolution of Problems

The team reviewed 246 Callaway Action Requests, several job orders, engineering evaluations,

associated root and apparent cause evaluations, and other supporting documentation to assess

problem identification and resolution activities. The team reviewed an additional 124 Callaway Action

Requests related to specific areas - essential service water, component cooling water, 480 Vac

auxiliary contacts and safety conscious work environment. Based on the sample selected for review,

the team concluded the licensee continued to have challenges in the area of prioritization and

evaluation, which require additional effort. The team also noted that licensee performance related to

problem identification and resolution had improved. The team determined the licensee had used the

self-assessment process and quality assurance organization to improve site performance. The team

determined the improvement resulted from corrective action process improvements implemented in

January 2007, and management oversight changes implemented following receipt of substantive

cross-cutting issue in problem identification and resolution.

The team determined that the licensee had initiated actions that improved the quality of their

operability assessments, operational decision-making, and knowledge of the detailed design and

licensing basis since the last evaluation. The graduated approach to assigning cause evaluations for

conditions adverse to quality and the change that required the Callaway Action Request screening

committee to review-all Callaway Action Requests provided increased assurance in the ability of the

licensee to identify and effectively resolve conditions adverse to quality.

The team determined that the licensee properly evaluated industry operating experience when

performing root cause and higher tier cause evaluations; however, the licensee had continued

challenges effectively evaluating industry operating experience.

The team determined that licensee audits and assessments continued to be detailed, probing, and

self-critical. The licensee continued to use benchmarking of industry best practices and third party

evaluations that improved the corrective action program performance during this assessment period.

The licensee had effectively implemented performance improvements to address the substantive

cross-cutting issue (refer to March 2, 2007, End of Cycle letter) related to evaluating actions required

for conditions adverse to quality as demonstrated by the decreased number of findings in the latter

half of this assessment period and lower affect that poor evaluations had on the facility. However,

the licensee will need to apply additional effort to affect improvements. The improving performance

resulted from increased management involvement in the corrective action program and in daily

activities.

-2- Enclosure

Because of the increased number of allegations at the facility in Calendar Year 2007, including

several discrimination concerns, the team interviewed more personnel than normal to assess the

safety conscious work environment at the Callaway Plant. The team documented the nature of the

concerns and the increased scope of the evaluations in Attachment 3. The team determined that not

all individuals were comfortable using all of the methods available 'to them for reporting concerns;

however, all personnel would have used at least one of the methods available for reporting a safety

concern. In addition, the team determined that the employee concerns program requires more

visibility and that not all personnel had confidence in the employee concerns program. The team

determined that our review results remained consistent with other safety culture surveys that

Callaway Plant had completed within the last year. The team determined that some general culture

and work environment issues continued to be present from the last assessment that were outside

NRC regulatory jurisdiction, which if not addressed could potentially affect the safety conscious work

environment at the Callaway Plant.

A. Inspector-identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. The team identified a Green noncited violation of 10 CER Part 50, Appendix B,

Criterion 1ll, "Design Control," because the licensee failed to ensure that Technical

Specification Surveillance Requirements for the NK1 1 and NK14 safety-related batteries

established limits that met the design requirements. Specifically, until questioned by the

team the licensee failed to determine the required design value needed to assure plant safety

as requested in Callaway Action Request 200706561. The licensee determined

that 69 micro-ohms should be the actual allowed inter-cell voltage limit to meet the design

requirements versus an allowed Technical Specification limit of 150 micro-ohms.

The performance deficiency associated with this finding involved the failure to ensure that the

NK1 1 and NK1 4 safety-related batteries would remain operable if all the inter-cell

connections measured 150 micro-ohms as allowed by Technical Specification Surveillance

Requirements 3.8.4.2 and 3.8.4.5. This finding was greater than minor because it was

associated with the Mitigating Systems cornerstone attribute of maintenance and testing and

affects the associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences.

Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of

Findings," the finding was determined to have very low safety significance because it was a

design deficiency confirmed not to result in loss of operability. The finding had a

cross-cutting aspect in the area of problem identification andiresolution associated with

operating experience because the licensee failed to evaluate in a timely manner relevant

internal and external operating experience P.2(a) (Section 40A2.e).

B. Licensee- Identified Violations

Violations of very low safety significance, which were identified by the licensee have been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have been

entered into the licensee's corrective action program. These violations and corrective actions

are listed in Section 40A7 of this report.

-3- -3-

Enclosure

REPORT DETAILS

4 w-16i ACTViTnES (OA)

-..-4OA2 Identification and Resolution of Problems

The team based the following conclusions, in part, on all issues that the team reviewed

during the assessment period, which ranged from November 1, 2006, to March 14, 2008.

The team divided the issues into two groups. The first group (current issues) included

problems identified during the assessment period where at least one performance deficiency

occurred during the assessment period. The second group (historical issues) included issues

identified during the assessment period but had performance deficiencies that occurred

outside the assessment period.

a. Assessment of the Corrective Action Program Effectiveness

(1) Inspection Scope

The team reviewed items from across the seven cornerstones to verify that the licensee:

(1) identified problems at the proper threshold and entered them into the corrective action

system, (2) adequately prioritized and evaluated issues, and (3) established effective and

timely corrective actions to prevent recurrence. The team performed field walk downs of the

component cooling water system and the 480 Vac breakers to inspect for deficiencies that

personnel should have entered into the corrective action program. The team reviewed

operator logs and station job orders to ensure personnel entered conditions adverse to

quality into the corrective action program. Additionally, the team reviewed a sample of

self-assessments, trending reports, system health reports, and various other documents

related to the corrective action program.

The team interviewed station personnel, attended screening committee, leadership and

Corrective Action Review Board meetings, and evaluated corrective action documentation to

determine the threshold for entering problems into their corrective action program. The

meetings assisted the team with their assessment of the threshold of prioritization and

evaluation of identified issues. The team performed a historical review of Callaway Action

Requests written over the last 5 years that addressed the component cooling water system

and the 480 Vac breakers.

The team reviewed plant records, primarily Callaway Action Requests and job orders, to

verify that the licensee developed and implemented corrective actions for identified problems,

including corrective actions to address common cause or generic concerns. The team

sampled specific technical issues to evaluate the adequacy of operability determinations.

Additionally, the team reviewed Callaway Action Requests that addressed past

NRC-identified and self-identified violations to ensure that the corrective actions addressed

the issues as described in the inspection reports. The team reviewed a sample of corrective

actions closed to other Callaway Action Requests, job orders, or other processes

to ensure that the licensee had appropriately implemented the corrective actions in a timely

manner.

-4- Enclosure

(2) Assessments

(a) Assessment - Effectiveness of Problem Identification

The licensee identified deficiencies as conditions adverse to quality and entered them into tim

corrective action program. From the inspection sample, the team identified only one example

for failure to identify excessive nuisance alarms as a condition adverse to quality.

Consequently, the licensee did not resolve the nuisance alarms in a timely manner.

Otherwise, the team determined that the licensee had established an appropriate threshold,

for identifying adverse conditions. The team determined that the licensee had lowered their

identification threshold, which improved their ability to identify conditions adverse to quality

during this assessment period. In addition, the team verified that the screening committee

evaluated all Callaway Action Requests to ensure that they identified any related adverse

condition no matter the Callaway Action Request type (i.e., adverse condition, business

tracking, training request, or request for resolution).

In response to the previous inspection, the team verified that the licensee had eliminated

Action Notices, which had resulted in violations during the previous inspection for various

reasons. The team verified that the licensee had appropriately evaluated open Action Notice

Callaway Action Requests to verify whether any adverse conditions required a cause

evaluation and more timely corrective actions. The team evaluated and found no instances

of a Significance Level 6 Callaway Action Request tracking an adverse condition. The

licensee had replaced the Action Notices with the business tracking Significance Level 6

Callaway Action Requests.

The team determined that licensee quarterly trend reports appropriately discussed and

tracked resolution of identified trends. The licensee recently initiated actions to lower the

threshold for identifying adverse trends so they could better utilize this tool to improve their

performance. The team verified that the licensee identified and recognized their adverse

trends, which represented improved performance since the last corrective action program

inspection.

Current Issues

Example: From interviews with security officers, the team determined that audible alarms on

a security feature sounded too often and decreased the sensitivity of the officers to monitor

the alarms as expected. The team determined that, although the security personnel and the

system engineer knew about the issue, no one had initiated a Callaway Action Request

documenting the excessive number of nuisance alarms. Officers had verbally reported and

sent e-mails to the system engineer who had contacted the vendor and made adjustments,

which had reduced, the alarms; however, the alarms continued. The team determined that

this deficiency was minor since the security feature remained capable of performing its

intended function. The licensee documented this deficiency in Callaway Action

Request 200801877.

-5- -5-

Enclosure

Historical Issues

Example 1: Licensee personnel failed to initiate Callaway Action Requests for conditions

adverse to quality, as required by 10 CFR Part 50, Appendix B, Criterion XVI. Documenting

these degraded conditions may have prevented a main steam line water hammer event in

June 2006 and may have identified, in August 2005, an additional high point air trap in the

Train A safety injection discharge piping that could impact system operability (NRC Inspection

Report 05000483/2006012-01).

Example 2: The team considered two Action Notice Callaway Action Requests (200602989

and 200608806), identified during this inspection, as inappropriately classified conditions

adverse to quality contrary to 10 CFR Part 50, Appendix B, Criterion V, and their corrective

action program (NRC Inspection Report 05000483/2006012-02).

Example 3: The licensee failed to identify three Action Notice Callaway Action Requests as

conditions adverse to quality (200603636, 200604166 and 200605466); however, the team

determined these examples represented minor findings.

Example 4: During audits from January 2005 through October 9, 2006, the licensee identified

63 Callaway Action Requests that personnel had initiated as action notices rather than

conditions adverse to quality. Quality Assurance issued Callaway Action Request 200606131

to document that personnel incorrectly listed six deficiencies as Action Notice Callaway Action

Requests instead of conditions adverse to quality. During review of the third quarter audit

data, the team identified an additional eight Action Notice Callaway Action Requests that the

audit process should have identified. This represented a 33 percent increase. The team

confirmed that the licensee had appropriately determined that personnel had misclassified

0.5 percent of the Action Notice Callaway Action Requests; however, the team verified none

of the misclassified items documented significant deficiencies.

Example 5: Plant operations and security had several prior opportunities to identify a

degraded fire door indicating personnel did not have a low threshold for identifying issues

(Inspection Report 05000483/2006005-01).

(b) Assessment - Effectiveness of Prioritization and Evaluation of Issues

The licensee did not always appropriately prioritize and evaluate conditions adverse to

quality. The team identified a large number of examples of poor evaluation that indicated

additional effort is needed in this area. Specifically, the team determined the licensee had:

two examples related to poor prioritization (Examples 1 and 3), two examples resulting from

personnel not fully implementing plant processes (Examples 2 and 8), one example of failure

to evaluate longstanding design issues (Example 6); and six examples that resulted from

ineffective evaluations (Examples 4, 5, 7, 9, 10 and 11). The team verified that the Callaway

Action Request screening process resulted in appropriately reassigning the significance level

of Callaway Action Requests commensurate with their safety significance (Example 12).

Similar to the last assessment, outside organizations continued to identify that the licensee

did not always perform effective evaluations of conditions adverse to quality; consequently,

the licensee continued to emphasize and provide management oversight. The licensee had

implemented product quality evaluations in Engineering. and had developed tools to evaluate,

-6- Enclosure

grade, and provide feedback on the Significance Level 1, Level 2 and selected Level 3

adverse condition Callaway Action Requests.

The team specifically evaluated the corrective actions related to operability evaluations and

root cause evaluations, which the last biennial problem identification and resolution inspection

identified as deficient areas. The team concluded that the actions taken by the licensee (e.g.,

reinforced expectations, training of engineers and operators in design and license bases and

performance of operability evaluations, and improved tiered root cause evaluation guidance)

had improved the quality of operability evaluations. However, the team determined the large

number of current examples for failure to adequately evaluate issues indicates the licensee

will need to take additional action in this area.

In response to external organization evaluations and as corrective action to the substantive

cross-cutting issue related to problem identification and resolution for inadequate evaluations

(refer to March 2, 2007, End of Cycle letter), the licensee initiated numerous actions to

strengthen the screening committee and other aspects of the corrective action program. A

majority of the actions related to reinforcing expected behaviors through coaching.

Current Issues

Example 1: As of December 19, 2007, the licensee had not tested the essential service

water, component cooling water and containment spray pumps at 20 percent of full flow.

Subsequently, the licensee invoked Surveillance Requirement 3.10.2 and completed the

testing within the extended 25 percent surveillance interval. While no violation of

requirements resulted, the licensee had not implemented the requirements in a timely

manner. The licensee documented this deficiency in Callaway Action Request 200801400.

Example 2: The resident inspector s determined the licensee performed an inadequate

post-maintenance test after repairing a damaged trip breaker contact block. Specifically,

personnel failed to identify that the contacts affected the P-4 interlock; consequently, the

licensee restored the breaker to service without performing a post maintenance test of the

P-4 interlock. Although this test failed to meet the requirements of 10 CFR Part 50,

Appendix B, Criterion Xl, the inspectors determined the violation was minor because the

licensee adequately tested the breaker prior to exceeding the Technical Specifications

allowed outage time. The licensee documented this deficiency in Callaway Action

Request 200800811.

Example 3: Quality assurance auditors documented in Callaway Action Request 200711176

that personnel had not properly re-screened Significance Level 6 Callaway Action

Request 200700560 to an adverse condition Significance Level 4 nor was a new adverse

condition identified once personnel determined that external operating experience applied to

Callaway Plant. The team concluded the deficiency was minor since no identified deficiency

resulted from the, review.

Example 4: Engineering approved deviating from the established motor-driven auxiliary

feedwater pump coupling tolerances provided by the vendor without considering the impact

on the thrust bearing (Inspection Report 05000483/2007004-02).

-7- -7-

Enclosure

Example 5: The resident inspectors determined that the licensee failed to evaluate the extent

of condition for micro-biologically induced corrosion of essential service water piping.

Specifically, the licensee failed to perform ultrasonic testing under the American Society of

Mechanical Engineers Code identification bands (Inspection Report 05000483/2007003-03).

Example 6: The resident inspectors determined that the licensee failed to evaluate a

longstanding ultimate heat sink cooling tower design issue, which resulted in allowing water

to flow over the fill below freezing conditions contrary to vendor recommendations (inspection

Report 05000483/2007003-01).

Example 7: The resident inspectors determined that the licensee failed to evaluate

micro-biologically induced corrosion of essential service water large-bore piping to ensure

the resolutions addressed causes and extent of condition (Inspection Report

05000483/2007002-03).

Example 8: After an operator could not locate a block switch during a surveillance test, the

control room supervisor revised *the procedure without verifying the correct block switch

identifier. Consequently, during the test when the operator defeated the identified (wrong)

train block feature, the opposite rain control room ventilation isolated (inspection

Report 05000483/2007002-01).

Example 9: Operations performed an inadequate review to establish compensatory actions of

an operator work around, which reflected a failure to thoroughly evaluate a problem to ensure

resolutions address causes and extent of condition (inspection Report 5000483/2006005-05).

Example 10: Engineering failed to thoroughly evaluate residual heat removal relief valve

problems to ensure resolutions addressed causes and extent of conditions (inspection

Report 05000483/2006009-06).

Example 11: Callaway Action Request 200801664 described that personnel failed to

document an adverse -condition that required evaluation. Specifically, after Quality Assurance

identified in Audit AP06-003 that the turbine-driven auxiliary feedwater pump exhaust line was

not adequately protected from missile hazards, Engineering initiated Request for

Resolution 2006006712; however, personnel failed to identify this as a potential

non-conforming condition in an adverse condition Callaway Action Request. Additionally, the

resident inspectors questioned if the current configuration was consistent with the licensing

basis.

Example 12: After reviewing significance level reassignments for Callaway Action Requests

that occurred during this assessment period, the team determined that the licensee had

appropriately classified the significance level for Callaway Action Requests and did not

identify a negative trend from this review. Specifically, for the population reviewed, the

licensee assigned a significance level to 65 items when no significance level had been

assigned, downgraded 25 items to a lower significance of which 15 received apparent cause

evaluations and 6 received a cause evaluation, and upgraded 53 items of which 34 received

cause evaluations.

-8- -8-

Enclosure

Historical Issues

Example 1: After questioning by the NRC, the licensee documented in Callaway Action

Requests 200609233 and 200500238 a less than adequate operability determination for a

degraded main steam isolation valve accumulator, which resulted in failure to implement the

required Technical Specification 3.7.2 actions (Inspection Report 05000483/2006012-03).

Example 2: The NRC determined that the licensee failed to properly evaluate and correct

inadequate emergency procedures for the design basis large break loss of coolant accident,

as documented in Callaway Action Requests 200602565 and 200608102. Specifically, the

licensee repeatedly missed opportunities that had presented themselves in Callaway Action

Requests, NRC findings, and vendor technical bulletins to uncover inadequate guidance in

Procedure E-1, "Loss of Reactor or Secondary Coolant" (Inspection

Report 05000483/2006011-01).

Example 3: The team determined that the licensee failed to evaluate all vulnerable

emergency core cooling system piping subject to voiding in response to a previous

NRC-identified violation for ineffective corrective actions. The team determined the licensee

failed to meet the requirements of 10 CFR Part 50, Appendix B, Criterion XVI. Specifically,

the licensee did not design and install vents for a significant length of horizontal piping

subject to the same deficiency and containing some high points, as documented in Callaway

Action Request 200608466 (Inspection Report 05000483/2006012-04)

Example 4: The Maintenance Rule Expert Panel failed to adequately review the failure of

safety-related motor-operated valves, which prevented thoroughly evaluating the problem to

ensure resolutions address causes and extent of conditions (Inspection

Report 05000483/2006005-02).

Example 5: Engineering performed an inadequate 10 CFR 50.59 safety evaluation, which

resulted in a less than thorough evaluation of the problem to ensure resolutions addressed

causes and extent of conditions (Inspection Report 05000483/2006005-04).

(c) Assessment - Effectiveness of Corrective Actions

The licensee implemented effective corrective actions to address conditions adverse to

quality because of process improvements. The team determined the improvements

addressed the weaknesses identified in the last biennial problem identification and resolution

inspection, as evidenced by only a single licensee-identified failure to implement effective

corrective actions. The team concluded that less than adequate past corrective action

program performance continued to result in the discovery of latent engineering issues; for

example, the ongoing challenges imposed by corrosion of the essential service water piping.

The team evaluated the planned actions for these corrosion deficiencies and concluded that

the licensee made appropriate operational decisions and took interim measures to ensure

that the system remained operable until the next refueling outage when they plan to

implement the permanent corrective actions.

The licensee had implemented a number of improvements in January 2007 that increased

the effectiveness of the corrective action program. The changes included, in part:

(1) improved definition of a condition adverse to quality in order to lower the threshold,

(2) more categories for adverse conditions to allow for broke-fix and relieve the burden of

-9- Enclosure

performing apparent causes for low significance conditions adverse to quality, (3) improved

guidance for performing cause evaluations, including a quality checklist, and (4)improved

guidance for performing immediate operability determinations. The team found that this

approach ensured the licensee applied the appropriate level of resources to identified issues

commensurate with their safety significance or impact on the facility. The team found the

procedure guidance clear, concise, and useful to personnel implementing the corrective.

action program. The team determined that many of these changes should address some of

the concerns identified during this inspection.

Current Issues

Example: The licensee determined that they had implemented ineffective corrective actions

for Callaway Action Request 200609621, which documented that personnel had failed to

secure Fire Door DSK1 5031. The corrective action involved communicating the importance

of reading and abiding to posted signs related to closing fire doors. Subsequently, additional

instances of the improperly secured fire door occurred (i.e., Callaway Action

Requests 200702037, 200702596, 200706810, and 200707100). After the license initiated

corrective actions for Callaway Action Request 200702596, which involved locking the door

pin to prevent unauthorized unlatching of the Fire Door DSK1 5031 stationary door, the

licensee had discovered two additional instances prior to implementing the modification., This

licensee-identified performance deficiency is documented in Section 40A7.

Historic Issues

Example 1: In Callaway Action Request 200609075, the licensee identified the failure to take

effective corrective actions in response to Callaway Action Request 200205928, which

documented missing sacrificial anodes in the emergency diesel generator heat exchangers.

The team determined the licensee had missed an opportunity to correct this deficiency in

October 2004. The failure to have all required sacrificial anodes installed was of minor safety

significance-since the heat exchanger remained operable.

Example 2: Callaway Action Request 200602995 described that personnel implemented

inappropriate corrective actions for Callaway Action Request 200602565. Specifically, the

NRC determined that the licensee made an ineffective procedure change related to

establishing component cooling water flow to the residual heat removal heat exchangers prior

to swap over to the containment recirculation sumps. The procedure change failed to prevent

a potential runout condition for the component cooling water pumps (inspection,

Report 05000483/2006011-02).

b. Assessment of the Use of Operating Experience

(1) Inspection Scope

The team examined licensee programs. for reviewing industry operating experience. The

team selected a number of operating experience notification documents (NRC bulletins,

information notices, generic letters, 10 CER Part 21 reports, licensee event reports, vendor

notifications, et cetera), which had been issued during the assessment period, to verify

whether the licensee had appropriately evaluated each notification for relevance to the

facility. The team then examined whether the licensee had entered those items, which had

been deemed relevant, into their corrective action program. Finally, the team reviewed a

_10- - 10 -Enclosure

number of significant conditions adverse to quality and conditions adverse to quality to verify

if the licensee had appropriately evaluated them for industry operating experience.

(2) Assessment

The team identified some weakness in licensee evaluation and processing of operating

experience. Specifically, failure to appropriately evaluate industry operating experience

contributed to two findings in this area. The team documented Example 1, which related to

untimely evaluation of applicable operating experience, in this inspection report. The team

determined that Example 2 documents failure to effectively evaluate operating experience

because the licensee did not consider all areas subject to flooding. Any finding that results

from the failure to perform an appropriate flood analysis will be documented in the resident

inspector integrated report. The team determined that the licensee continued to effectively

assess industry operating experience during root cause and apparent cause evaluations of

significant conditions adverse to quality and conditions adverse to quality, respectively.

Current Issues

Example 1: The team determined that the licensee failed to determine in a timely manner

whether the acceptance criteria for Technical Specification Surveillance Requirement 3.8.4.5

demonstrated that the NK1 1 and NK14 safety-related batteries could meet the design

requirements. The licensee initiated Callaway Action Request 200706268 in response to

operating experience on July 10, 2007. The licensee inappropriately requested extension

requests to complete their evaluation such that they had operated with this non-conservative

Technical Specification until challenged by the team -(refer to Section 40A2.e).

Example 2: In Callaway Action Requests 200502989 and 200607843, the licensee

concluded that the flooding analysis summary took no credit for flooding in areas above the

lower levels in each building. The team considered the evaluation inadequate because

several flooding analyses credit floor drains at elevations other than the-*basement. For

example, Calculation. M-FL-07, "Flooding of the Aux Bldg Rms EL. 2047'6",' evaluated the

impact of flooding in the Control Room heating, ventilation and air conditioning room.

Historical Issues

Example: The licensee's corrective measures inappropriately used instrument uncertainty to

increase design margin (inspection Report 05000483/2006009-05).

C. Assessment of Self-Assessments and Audits

(1) Inspection Scope

The team reviewed numerous audits, self-assessments, quality surveillances, and site

performance indicators. The team reviewed program procedures and interviewed process

managers related to the performance improvement group, the corrective action program, and

the Quality Assurance department. The team evaluated the use of self- and third party

assessments, the role of Quality Assurance, and the role of the performance improvement

group related to licensee performance.

- 11 - -11-

Enclosure

(2) Assessment

The licensee continued to perform self-critical assessments, audits and evaluations. The

team noted that the factors that influenced the improvement identified during the last

corrective action program evaluation continued during this assessment period. Specifically,

the licensee used directed assessments to evaluate suspect or known areas of weakness.

The licensee implemented the recommendations and findings of external self-assessments

that they requested. The licensee established processes to ensure increased management

oversight at all levels in the organization related to improved worker performance, adherence

to procedures, and conduct of root cause analyses.

Quality Assurance performed critical, detailed audits and surveillances of line

organizations (Example 2). The audit performance criteria had goals of excellence (e.g., third

party expectations and NRC inspection guidance) rather than compliance. The team

determined that the line organizations continued to use audits and surveillances as a tool to

improve their performance. For example, Quality Assurance performed three surveillances of

critical activities related to the corrective actions planned for the essential service water

system corrosion issues (Example 1).

The team verified that the licensee implemented performance indicators and trended data

that should allow the managers to evaluate the progress of their actions to improve

performance related to human performance and corrective action program deficiencies.

The licensee performed several self-assessments related to safety culture during this

assessment period. The team evaluated the self-assessments and concluded that the

licensee conducted critical evaluations of their safety culture and the safety conscious work

environment (Examples 3 and 4). The licensee initiated Callaway Action Request 200800944

to perform a higher tier apparent cause evaluation and to ensure that they addressed the

assessment recommendations. Recommendations included developing a differing

professional opinion process, developing a process to review proposed disciplinary actions

and performing benchmarking of other programs.

Current Issues

Example 1: Quality Assurance performed several critical surveillances related to corrosion in

the essential service water system, which related to the examination scope of the piping, the

repairs of the affected piping, and the suitability to operate during Cycle 16.

Example 2: Audit AP07-013, "Corrective Action Program," provided critical evaluations of the

corrective action program areas that previously had problems, which included operability

evaluations, prioritization, and management oversight. The team verified that the line

organization had implemented appropriate corrective actions to address the numerous

adverse conditions identified in the audit.

Example 3: The licensee performed a Synergy Safety Culture Assessment in February 2007.

The Safety Culture Survey included an assessment of the general culture and work

environment and the safety conscious work environment. The safety culture survey identified

that the licensee had significant challenges related to resources/work load and change

management that affected the trust of the workers in management. The survey identified that

no chilling effect or safety conscious work environment concerns existed. However, the

-12- Enclosure

results indicated, the general culture and work environment concerns could affect the nuclear

safety culture and the safety conscious work environment, if not addressed by management.

Example 4: Because of the large number of allegations at the facility in Calendar Year 2007,

the licensee requested an independent assessment to evaluate their safety conscious work

environment in February 2008. The assessment determined that the licensee had

maintained a safety conscious work environment and that no chilled work environment

existed. The assessment team concluded work environment and corrective action program

issues had the potential, if not addressed, to erode the willingness of individuals to bring

issues forward using the corrective action program.

d. Assessment of Safety Co nscious Work Environment

(1) Inspection Scove

The team evaluated this area by reviewing self-assessments and audits, interviewing

personnel regarding the safety conscious work environment at Callaway Plant using the

questions provided in Inspection Procedure 71 152B, and interviewing the Employee

Concerns Coordinator. Specifically, the-team reviewed the Independent Assessment of the

Callaway Plant Safety Conscious Work Enviro~nment performed in February 2008, the 2007

Safety Culture Assessment, and three department specific safety culture assessments.

The team conducted formal interviews with 93 personnel in response to the large number of

allegations received at Callaway Plant, which had identified concerns with the safety

conscious work environment. Normally, the inspection interviews 15 -25 personnel. The

team conducted the interviews with plant personnel to assess their willingness to raise safety

issues and use the corrective action program. Further, the team assessed whether

conditions existed that would challenge the establishment of a safety-conscience Work

environment. The team documented the details of the review in Attachment 3, "Concerns

Evaluated." Note: Examples 1 - 5 below have corresponding numbers in Attachment 3.

() Assessment

From interviews and review of safety conscious work environment assessments, the team

determined that the licensee maintained a safety conscious work environment. However,

there were some issues identified that were outside NRC regulatory jurisdiction that, if not

addressed by the licensee, could potentially affect the safety conscious work environment at

the Callaway Plant. Overall, interviewed employees felt free to enter issues into the

corrective action program as well as, raise nuclear safety concerns to their supervision, the

employee concerns program, and the NRC. During interviews, personnel generally

expressed confidence that the licensee had established an appropriate threshold for

documenting nuclear safety issues and that issues entered into the corrective action program

would be appropriately addressed.

The 2007 Safety Culture Assessment concluded that the licensee,, generally, has a solid

safety culture and that site personnel have nuclear safety as a core value. However, the

safety culture assessment identified several groups that required additional attention. The

assessment also identified areas that management needed to address related to the general

culture and work environment that included implementing appropriate change management,

better management of resources, workload, staffing and priorities. The team verified that the

-13- - 13-Enclosure

licensee had initiated Callaway Action Requests and had implemented appropriate corrective

actions for the identified deficiencies.

Consistent with the 2005 Safety Culture Assessment, the 2007 Safety Culture Assessment,

and the February 2008 Safety Conscious Work Environment self-assessment, the team

determined that, generally, employees expressed willingness to use the corrective action

program and raise nuclear safety concerns. The team determined that not all individuals

were comfortable using all of the methods available to them for reporting concerns; however,

all personnel would have used at least one of the methods available for reporting a safety

concern. Also, the licensee continues to have challenges related to visibility of the Employee

Concerns Program and the willingness of some people to use the Employee Concerns

Program (Examples 2 and 3).

In response to numerous concerns (Examples 1 - 3) the team evaluated whether the

licensee encourages personnel to identify problems. The team determined that management

encourages personnel to identify problems and raise concerns using the corrective action

program or through discussions with their supervisor. The team determined from this sample

that no chilled work environment existed at Callaway Plant. However, within the security

department, some individuals would not raise personal concerns. From review of two

technical concerns (Examples 4 and 5), the team determined that the licensee had resolved

the issues commensurate with their safety significance and regulatory requirements.

Current Issues

Example 1: The team evaluated whether the licensee had established a culture where

personnel did not feel comfortable raising concerns and where management did not want to

hear about problems. The team determined that management encouraged personnel to

raise concerns. During interviews, all personnel indicated that they would raise nuclear

safety concerns; however, some personnel indicated that they would not raise personal

issues unrelated to nuclear safety because they believed that management would take no

actions.

Example 2: The team evaluated how employees used the employee concerns program. The

team determined that most, but not all, employees would use the employee concerns

program if they did not get satisfaction from use of the corrective action program or from their

supervisor. However, two individuals did not trust the employee concerns program and would

rather talk to the NRC. The team determined that 30 percent of the personnel interviewed

had a misconception of the employee concerns program (e.g., did not know the program

coordinator had changed, did not know the purpose of the employee concerns program, did

not know the location of the coordinator's office, et cetera).

Example 3: The team evaluated whether a chilled work environment existed in any

department but focused particularly in the training, radiation protection, operations and

security organizations. From the interviews, the team determined that all individuals would

raise concerns by using one of the four methods - corrective action program, supervisor,

employee concerns program, or NRC. However, the team determined that not all individuals

would use all of the methods. Specifically, one individual would only talk with their supervisor.

Example 4: The team reviewed whether the licensee timely resolved the condition that

damaged to the residual heat removal pump suction relief valves. The licensee missed an

-14- Enclosure

opportunity to correct the error in March 2007 when a design error identified by a vendor

prevented issuing the modification in time for implementation. The team verified that the

licensee scheduled the modification for Refueling Outage 16 in October 2008. No violation

resulted since the licensee will implement the modification commensurate with its safety

significance.

Example 5: The team reviewed whether the licensee took the appropriate actions to not

pursue a license amendment specifically prohibiting plant operation with both cold

overpressure mitigation systems out of service with the reactor coolant system solid. Since

the licensee had no shutdown probabilistic safety \analysis, the team could not quantitatively

determine whether it was safer to operate without cold overpressure mitigation system valves

under solid plant conditions or saturated plant conditions. Further, the team determined that

the licensee took appropriate actions to request an extension of the period allowed for

establishing a reactor coolant system vent path from 8 to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Example 6: As discussed. in the example in Section 40A2.a(2)(a), security officers had

identified that a specific security feature generated excessive nuisance alarms. The team

determined that the licensee had initiated Callaway Action Requests related to other security

organization issues that included a safety hazard while performing patrols and a health

hazard. The team determined during interviews that these deficiencies did not aff ect the

willingness of security officers to report deficiencies to their supervisor or to use the corrective

action program.

e. Specific Issues Identifiled During This Inspection

Introduction. The team identified a Green noncited violation of 10 CFR Part 50, Appendix B,

Criterion Ill, "Design Control," because the licensee failed to ensure that Technical

Specification Surveillance Requirements for the NK1 1 and NK14 safety-related batteries

established limits that met the design requirements. Specifically, until questioned by the

team the licensee failed to determine the required design value needed to assure plant

safety. The licensee determined that 69 micro-ohms should be the actual allowed inter-cell

voltage limit to meet the design requirements versus an allowed Technical Specification limit

of 150 micro-ohms.

Description. The team reviewed Callaway Action Request 200706561 that the licensee

initiated July 10, 2007, to evaluate the adequacy of Technical Specifications 3.8.4 and 3.8.5

for the NK1 1 and NK1I 4 safety-related batteries. The licensee initiated Callaway Action

Request 200706561 because external industry operating experience had identified that some

licensees had not documented the basis for the 150 micro-ohm limit specified in Technical

Specification Surveillance Requirements 3.8.4.2 and 3.8.4.5 and, in some cases, challenged

the operability of the safety-related batteries when the limit was applied to each inter-cell

connection. Callaway Action Request 200706561, Action 4 requested an evaluation to

determine the appropriate maximum inter-cell resistance value for station batteries. The

team determined that the licensee had not completed their evaluation of Surveillance

Requirements 3.8.4.2 and 3.8.4.5 at the time of the inspection.

The team determined that Procedure APA-ZZ-01400, Attachment 4, "Industry Operating

Experience Screening Committee Guidelines," Section 4.b, states that Operating Experience

.Callaway Action Requests should be assigned due dates not to exceed 60 days to ensure a

timely determination of plant impact. The team determined that, while the licensee had

_15- - 15-Enclosure

assigned a completion date within 60 days, personnel had obtained several extensions that

prevented assessing the significance or facility impact within the initial 60 days specified in

Procedure APA-ZZ-01400. Consequently, these extensions delayed evaluating Surveillance

Requirements 3.8.4.2 and 3.8.4.5. Following discussion with the team, the licensee

evaluated the current design assumptions in Calculation NK-05, "Class 1E Battery Capacity;"

Revision 6, which the licensee had used to size the NK1 1 and NK14 safety-related batteries.

The licensee's evaluation found that the licensee based the battery sizing on an end

discharge voltage of 108.6 volts correlating to a maximum inter-cell resistance of 86.1

micro-ohms. Since the 86.1 micro-ohms limit was less than that allowed by Surveillance

Requirements 3.8.4.2 and 3.8.4.5 (indicating a nonconservative Technical Specification), the

licensee performed an additional calculation to determine an appropriate inter-cell resistance

to support battery operations. Upon completing Calculation NK-10, "NK1 1 Accident Case,"

Revision 1, the licensee would need to limit the maximum inter-cell resistance to

69 micro-ohms to assure battery operability.

Following discovery of the non-conservative inter-cell resistance, the licensee performed a

prompt operability determination and concluded the NK1 1 and NK1,4 safety-related batteries

remained operable since past surveillances had measured inter-cell resistances well below

69 micro-ohms. The licensee implemented compensatory measures as described in NRC

Administrative Letter 1998-10, "Dispositioning of Technical Specifications That Are

Insufficient to Assure Plant Safety," to assure the new inter-cell resistance limit of

69 micro-ohms would not be exceeded. The licensee intended to continue the interim

compensatory measures until they revised their Technical Specifications.

Analysis. The performance deficiency associated with this finding involved the failure to

ensure that the NK1 1 and NK14 safety-related batteries would remain operable if all the

inter-cell connections measured 150 micro-ohms as allowed by Technical Specification

Surveillance Requirements 3.8.4.2 and 3.8.4.5. This finding was greater than minor because

it was associated with the Mitigating Systems cornerstone attribute of maintenance and

testing and affects the associated cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and

Characterization of Findings," the finding was determined to have very low safety significance

because it was a design deficiency confirmed not to result in loss of operability. The finding

had a crosscutting aspect in the area of problem identification and resolution associated with

operating experience because the licensee failed to evaluate in a timely manner relevant

internal and external operating experience P.2(a).

Enforcement. Title Ten Code of Federal Regulations Part 50, Appendix B, Criterion Ill,

"Design Control," requires, in part, that the licensee establish measures to assure that

applicable regulatory requirements and the design basis for structures, systems and

components are correctly translated into specifications, drawings, procedures, and

instructions. Additionally, design control measures shall provide for verifying or checking the

adequacy of design, such as by the performance of design reviews, by the use of alternate or

simplified calculation methods, or by the performance of a suitable testing program. Contrary

to the above, prior to March 13, 2008, the licensee failed to verify that the 150 micro-ohm

criterion specified in Surveillance Requirement 3.8.4.2 and 3.8.4.5 would be sufficient to

ensure safety-related battery operability in accordance with the design basis. Once

challenged, the licensee determined that a maximum inter-cell resistance of 69 micro-ohm

could not be exceeded to ensure the battery remained operable. This finding is of very low.

-16- Enclosure

safety significance and has been entered into the corrective action program as Callaway

Action Request 200802195, this violation is being treated as a noncited violation consistent

with Section VI.A of the NRC Enforcement Policy: NCV 05000483/2008006-01,

"Nonconservative Technical Specification for battery inter-cell connection resistances."

40A6 Exit Meeting

On March 14, 2008, the team presented their inspection results to Mr. A.C. Heflin, Vice

President, and other members of his staff who acknowledged the findings. The inspectors

returned all proprietary and confidential information p~rovided during the inspection.

40A7 Licensee Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee

and is a violation of NRC requirements that meets the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as a noncited violation.

Technical Specification 5.4.1 .d requires that AmerenUE maintain a fire protection program.

Procedure APA-ZZ-0071, "Control of Impairments of Fire Protection Systems and

Components," requires personnel to maintain the integrity of plant fire doors. Contrary to

this, security officers identified during routine tours on March 6, March 20, July 18, and

July 31, 2007, which personnel failed to maintain the integrity of Fire Door 15031. This

licensee documented these deficiencies in Callaway Action Requests 200702037,

200702596, 200706810, and 200707100, respectively. This finding is of very low safety

significance because the exposed fire area contained no potential damage targets that are

unique from those in the exposing fire area.

Attachment: Supplemental Information

-17- Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

B. Barton, Manager, Training

G. Belchik, Supervisor, Operations

M. Daly, Supervising Engineer, Corrective Action Program

F. Diya, Plant Director

M. Dunbar, Protective Services Supervisor

R. Farnam, Manager, Radiation Protection

L. Graessle, Manager, Regulatory Affairs

A. Heflin, Vice President - Nuclear

T. Herrmann, Vice President Engineering

T. Hermann, Manager, Maintenance

D. Hollabaugh, Superintendent Protective Services

L. Kanuckel, Manager, Quality Assurance

G. Kremer, Supervising Engineer

P. McKenna, Manager, Outage Planning and Scheduling

M. McLachlan, Manager, Engineering Services

S. Maglio, Assistant Manager, Regulatory Services

B. Miller, Supervisor, Performance Improvement

E. Olsen, Superintendent, Performance Improvement

S. Petzel, Engineer, Regulatory Affairs

J. Small, Superintendent, Chemistry and Radioactive Waste

T. Steele, Employee Concerns Program Coordinator

NRC

R. Caniano, Director, Division of Reactor Safety (telephonically)

J. Groom, Resident Inspector, Callaway Plant

L. Smith, Chief, Engineering Branch 2, Division of Reactor Safety

V. Watkins, Deputy Director, Division of Reactor Safety

LIST OF ITEMS OPENED AND CLOSED

Opened and Closed

05000483/2008006-01 NCV Nonconservative Technical Specification for Battery

Inter-cell Connection Resistances (Section 40A2.e)

A1-1 Attachment 1

LIST OF DOCUMENTS REVIEWED

Audits, Self-Assessments and Surveillances

AP07-013, "Quality Assurance Audit of Corrective Action," dated December 13, 2007

SA07-Pl-C02, "Closing Condition Reports (CARS) to a Procedure Change Process,"

dated August 28, 2007

SA07-PI-C06, "Trending Program Gap Analysis," dated August 2007

SA07-PI-F01, "Mid-Cycle Self-Assessment," dated September 10-21, 2007

SA07-PI-S01, "Gap Analysis between APA-ZZ-01 400 and INPO 05-005," dated June 6, 2007

SA07-PI-S02, "Prompt Human Performance Evaluation," dated May 23, 2007

SA07-PI-S05, "Assessment of the Self-Assessment Program during the Mid-Cycle

Self-Assessment," dated October 25, 2007

SP07-001, "Assess Engineering Dispositions of Significance Level 3 CARs,"

dated February 15, 2007

SP07-013, "Assure ESW Piping Has Been Determined Suitable for Continued Operations,"

dated April 3, 2007

SP07-015, "Assessment of Corrective Actions for ESW Pipe Support Removal,"

dated April 11, 2007

SP07-020, "Assess ESW Examination Plans and Methods during RF15 to Address Large Bore

Pipe Pitting and Ensure Reliability during Cycle 16," dated April 13, 2007

SP07-021, "Overview of the Refuel 15 Human Performance Area," dated June 6, 2007

SP07-025, "Evaluate Refuel 15 ESW Repair/Replacement Activities," dated May 21, 2007

SP07-035, "Evaluate Adequacy of Responses to Audit AP06-006, 'Design Control,"'

dated September 25, 2007

Calculations

EB-10, "Allowable MCC circuit lengths for circuits with auxiliary relay coils in parallel with the

starter coil," Addendum 1, Revision 0

EJ-039, "Maximum Vent Times for Points Vented in Procedure OSP-SA-00003," Revision 0

KJ-10, "Determine Tube Plugging Limits for DG Intercooler Heat Exchangers, DG Jacket Water

Heat Exchangers and the Lube Oil Coolers," Revision 0

All-2 Attachment 1

R-41 52-00-1, "Revised Maximum Vent Volumes for EMV0250, EMVO251, and EMV0252 vent

points," Revision 0

ZZ-1 79, "Plant AC Load List," Revision 7

Callaway Action Requests

200203882 200608956 200700284 200702529 200705936 200709330

200306252 200608979 200700286 200702568 200705968 200709522

200 502093 200609233 200700392 200702596 200706133 200709523

200505716 200609441 200700560 200702685 200706143 200709540

200509540 200609580 200700893 200702864 200706268 200709652

200600012 200609603 200700956 200702956 200706453 200709812

200602144 200609621 200701164 200703065 200706476 200709813

200602645 200609628 200701177 200703069 200706561 200709819

200603734 200609710 200701261 200703177 200706810 200709852

200603736 200609726 200701336 200703189 200706933 200710351

200604147 200609805 200701362 200703244 200707100 200710418

200604872 200609809 200701369 200703260 200707368 200710764

200604878 .200609809 200701371 200703317 200707375 200711084

200604991 200609812 200701372 200703901 200707468 200711176

200605025 200609813 200701406 200704101 200707485 200711177

200605046 200610010 200701407 200704113 200707490 200711227

200605143 200610048 200701559 200704169 200707508 200711235

200605179 200610063 200701573 200704176 200707518 200711236

200605252 200610112 200701591 200704226, 200707572 200711254

200605751 200610359, 200701654 200704366 200707628 200711257

200605879 200610423 200701660 200704472 .200707788 200711314

200606432 200610426 200701930 200704598 2007081 22 200711496

200606707 200700023 200701944 200704742 200708186 200711541

200607188 200700063 200702003 200704911 200708219 200711883

200607327 200700096 200702037 200704913 200708233 200711916

200607496 200700100 200702057 200705117 200708241 200800085

200607835 200700115 200702144 200705142 200708270 200800248

200607843 200700218 200702202 200705149 200708671 200800585

200607911 200700224 200702276 200705263 200708941 200800878

200607985 200700260 200702339 200705349 200709002 200801268

200608466 200700262 200702371 200705484 200709165 200801664

200608902 200700265 200702373 200705489 200709171 200801877

Jobs

05104004 05506731 06129999 07007930 07008908

Al -3 A1-3

Attachment 1

Requests for Resolution

200706500 200701932

Callawav Action Reauests Sionificance Level 4 Reviews

Ac

........... in ea t . e Leve

. .. 4.... . ..

Reviews.. .

.........

200700815 200706812 200708769 200709845 200711009 200711696

200700839 200707147 200708778 200709868 200711028 200711741

200702456 200707184 200708873 200709894 200711036 200711831

200703494 200707250 200708942 200709959 200711067 200711955

200705711 200707294 200709232 200710139 200711378 200712005

200706212 200708020 200709657 200710446 200711481 200800007

200706427 200708062 200709660 200710537 200711543 200800152

200706571 200708068 200709698 200710915 200711647 200800205

200706688 200708435 200709740 200710923 200711662 200800226

Callawav Action Reoue~t~ reviewed for comnonent . ..

coolina

.

water 55-year

... in i w ater. ...........

review

C allaw ay .......... o

Aci en ... t ... .. ... for .. . .. r-..

200300081 200302684 200402981 200500662 200509277 200800740

200300176 200306225 200407285 200502438 200510023

200300762 200306229 200408368 200504816 200601037

200300767 200306380 200408434 200507430 200602580

200300837 200307361 200408696 200507574 200604400

200301779 200401270 200500143 200507684 200710764

Callaway Action Requests related to essential service water

200600553 200702464 200703247 200703899 200704785 200707154

200608086 200702496 200703279 200704226 200705002 200710009

200701786 200702724 200703313 200704366 200705126 200710571

200702151 200702733 200703514 200704421 200705489

200702384 200703028 200703584 200704465 200705535

200702434 200703222 200703776 200704598 200706190

Information used to evaluate 480 Vac auxiliary contacts

200400789 200509628 200404059 200604013 200404301

200404392 200607324 200404486 200609726

200405034 200704719 200507793 200709688

Auxiliary Contacts Failure Trending

Replacement Timeline for NG 480 Vac Buckets

Project Plan MP01-1003/21130, "Replace Obsolete MCC Buckets (starters and aux contacts),"

dated February 5, 2008

Al1-4 Attachment 1

Procedure CC-74-14, "IEEE 323-1974, "Qualification and Test Summary Report for Class IE Motor

Control Centers," Revision 6

Procedures

APA-ZZ-00107, "Review of Current Industry Operating Experience," Revision 10

APA-ZZ-00304, "Control of Callaway Equipment List," Revision 23

APA-ZZ-00322, "Integrated Work Management Process Description," Revision 3

APA-ZZ-00500, "Corrective Action Program," Revisions 44 and 45

APA-ZZ-00500, Appendix 1, "Operability and Functionality Determinations," Revision 4

APA-ZZ-00500, Appendix 5, "Maintenance Rule (MR)," Revision 2

APA-ZZ-00500, Appendix 7, "Effectiveness Reviews," Revision 2

APA-ZZ-00500, Appendix 12, "Significant Adverse Condition - Significance Level 1," Revision 1

APA-ZZ-00500, Appendix 13, "Adverse Condition - Significance Level 2," Revision 1

APA-ZZ-00500, Appendix 14, "Adverse Condition - Significance Level 3," Revision 2

APA-ZZ-00500, Appendix 15, "Adverse Condition - Significance Level 4," Revision 3

APA-ZZ-00500, Appendix 16, "Adverse Condition - Significance Level 5," Revision 2

APA-ZZ-00500, Appendix 17, "Screening Process Guidelines," Revision 4

APA-Z7Z-00500, Appendix 21, "Other Issues - Significance Level 6," Revision 2

APA-ZZ-0500A, "Business Tracking Process," Revision 5

APA-ZZ-00604, "Requests for Resolution," Revision 20

APA-ZZ-00930, "Employee Concerns Program," Revision 10

APA-ZZ-01250, "Operational Decision Making," Revision 1

APA-ZZ-01400, "Performance Improvement Program," Revision 6

APA-ZZ-01400, Appendix E, "Operating Experience," Revision 3

APA-ZZ-01400, Appendix F, "Performance Indicators," Revision 2

APA-ZZ-01400, Appendix J, "Change Management," Revision 5

EDP-ZZ-01 112, "Heat Exchanger Predictive Performance Manual," Revision 13

EDP-ZZ-0 1128,. "Maintenance Rule Program," Revision 8

EDP-ZZ-01 131, "Callaway Plant Health Program," Revision 9

EDP-ZZ-05000, "Engineering Product Quality," Revision 3

LDP-ZZ-00500, "Corrective Action Review Board," Revision 10

ODP-ZZ-00001, Addendum 12, "Operator Burdens and Workarounds," Revision 0

TDP-ZZ-00076, "Training Department Self-Assessment Process," Revision 4

TDP-ZZ-00075, "Training Department CARB," Revision 5

Miscellaneous

Change Package MP 07-0066, "Replace Buried ESW Piping with HDPE Material," Revision 0

Callaway Plant 3d Quarter and 4 th Quarter Trend Reports

Health Risk EF-03-07, "Corrosion of Large Bore ESW Piping - ESW Flow Only (Includes

Underground)"

Letter ULNRC-05434, "10 CFR 50.55a Request: Proposed Alternative to ASME Section Xl

Requirements for Replacement of Class 3 Buried Piping," dated August 30, 2007

A1-5 Attachment 1

Letter ULNRC-05445, "Application for Amendment to Facility Operating License NPF-30,

One-Time Completion Extension for Essential Service Water (ESW) System,"

dated October 31, 2007

Proto-Power Corporation Letter to Alex Smith, "Callaway Plant Heat Exchange Engineer, RE:

Summary of GL 89-13 Program Review," dated December 21, 2006

Training Excellence Plan 2008- 2012, dated February 7, 2008

Safety Conscious Work Environment

Callaway Plant Business Plan 2008 -2012

Employee Concerns Program Pamphlet

NEI 97-05, "Nuclear Power Plant Personnel-Employee Concerns Program-Process Tools in a

Safety Conscious Work Environment," Revision 2

Nuclear Division Policy POLOO17, "Safety Conscious Work Environment Policy," Revision 2

Procedure SDP-PI-DEFNS, "Static Defensive Position," Revision 1

Procedure APA-ZZ-00930, "Resolving Quality Concerns," Revision 4 (10/30/2004)

Regulatory Issue Summary 2005-18, "Guidance for Establishing and Maintaining a Safety

Conscious Work Environment," dated August 25, 2005

Regulatory Issue Summary 2006-13, "Information on the Changes Made to the Reactor Oversight

Process to More Fully Address Safety Culture," dated July 31, 2006

SEGR 07-34, "QA Department Detailed Evaluation of SynergyNPO Results,"

dated November 2, 2007

SEGR 07-35, "INPO SOER 02-04 Davis Besse CBT," dated November 16, 2007

Understanding SCWE - A Handbook on Safety Conscious Work Environment

As the Turbine Turns Articles on Principles for a Strong Nuclear Safety Culture (dated November

and December 2006)

"An Independent Assessment of the Safety Conscious Work Environment at the Callaway Nuclear

Plant," dated February 1, 2008

2005 and 2006 Allegation Trends Report evaluations related to the Callaway Plant

2006 Operations, Engineering and Training department NEI/USA safety conscious work

environment questionnaires

A1-6 Attachment 1

2007 Safety Culture Survey

Callaway Action Reauests reviewed related to safety conscious work environment

200404503 200502693 200601951 200610290 200706425

200406409 200502722 200604086 200706407 200706429

200407284 200504133 200604672 200706417 200707744

200407480 200506261 200606421 200706418 200708271

200408626 200601104 200606424 200706420 200800944

200501049 200601108 200607472 200706421

200501953 200601377 200609882 200706423

Anonymous Callaway Action Requests

200500861 200502772 200600955 200701820 200711093

200500862 200503740 200604751 200709845 200711543

200500679 200504155 200605954 200710703

All-7 Attachment 1

Attachment 2

Initial Information Request - December 26, 2007

Callaway Problem Identification and Resolution Biennial Inspection

(IP 71152B; Inspection Report 05000483/2008006)

The inspection will cover the period of August 1, 2006, to February/March 2008. All requested

information should be limited to this period unless otherwise specified. As discussed, you can

upload the information to the Certrec inspection website. We would also like the information

provided on a CD prior to our preparation week. We will break down the request by required dates

to allow for effective preparation. Information provided in electronic media may also be in the form

of e-mail attachment(s), CDs, or thumb drives. The Agency has converted to MSOff ice. We have

document viewing capability for Adobe Acrobat (.pdf) files and other image files.

Please have the information uploaded to the Certrec Website by January 25, 2008, if possible.

Note: On summary lists please include a description of problem, status, initiating date, and

owner organization. Since you had a major conversion of your significance categories in

January 2007, the team would like to have the requests divided, as necessary so that the

information requested is compatible as far as significance. If you had existing CARS that

were converted from the old system to the new system a list of those converted would be

convenient.

1. Summary list of all Callaway Action Requests (CARS) of significant conditions adverse to

quality (Significant level 1 and 2) opened or closed from 08/01/2006 thru the conversion

implementation and (Significance Level 1, 2, and 3) after the conversion to the present.

2. Summary list of all CARS which were generated since 08/01/2006 separated by those prior

to the conversion and following the conversion

3. A list of all corrective action documents that aggregate or "roll-up" one or more smaller

issues for the period

4. Summary list of all action requests which were down-graded or up-graded in significance

since 08/01/2006

5. List of all root cause analyses completed since 08/01/2006. Include in this listing those root

causes considered as upper tier cause evaluations.

6. List of root cause analyses planned, but not complete at end of the period, include in this

list the upper tier cause evaluations.

7. List of all apparent cause analyses completed since 08/01/2006.

8. List of plant safety issues raised or addressed by the employee concerns program since

08/01/2006

A2-1 Attachment 2

9. List of action items generated or addressed by the plant safety review committees since

08/01/2006

10. All quality assurance audits and surveillances of corrective action activities completed since

08/01/2006

11. A list of all quality assurance audits and surveillances scheduled for completion since

08/01/2006, but which were not completed

12. All corrective action activity reports, functional area self-assessments, and non-NRC third

party assessments completed since 08/01/2006

13. Corrective action performance trending/tracking information generated since 08/01/2006

and broken down by functional organization. Quarterly reports are sufficient for this area if

they are broken down by organization and issue.

14. Current revisions of corrective action program procedures for: Condition Reporting,

Corrective Action Program, Root Cause Evaluation/Determination, Operator Work

Arounds, Work Requests, Requests for Engineering Resolution (RFR), Temporary

Modifications, Procedure Change Requests, Deficiency Reporting and Resolution,

Operating Experience Evaluation

15. A listing of all external events (OE) evaluated for applicability at Callaway since 08/01/2006

16. Action requests or other actions generated since 08/01/2006 for each of the items below:

Part 21 Reports:

[Applicable] NRC Information Notices:

All LERs issued by AmerenUE

NCVs and Violations issued to AmerenUE (including licensee-identified violations)

17. Safeguards event logs

18. Current system health reports or similar information

19. -Current predictive performance summary reports or similar information

20. Corrective action effectiveness review reports generated since 08/01/2006

21. List of risk significant components and systems

22. List of actions done and/or in the Human Performance Improvement Plan since the last

PIR inspection

23. Outage maintenance that was not done for whatever reason.

24. Any rework of maintenance performed from last outage

A2-2 Attachment 2

Attachment 3 - Concerns Evaluated

The NRC received a large number of allegations in Calendar Year 2007 at the Callaway Plant.

Consequently, Region IV management requested the biennial problem identification and resolution

inspection team to conduct a larger than normal number of safety conscious work environment

interviews. The team grouped these concerns into three major areas (Examples 1 - 3) that

reflected the types of statements made regarding the Callaway Plant. The team also reviewed two

technical concerns (Examples 4 and 5).

Example 1 - General Culture Concerns:

  • Callaway Plant has a culture that discourages disagreement with upper management and

inhibits effective problem identification and resolution. (Operations)

" Management would prefer not to know about problems and is reluctant to fully investigate

them. (Operations)

  • Workers do not enter issues into the corrective action program because they will be tasked

with resolving the issues. (Radiation Protection)

  • Callaway does not have a healthy safety conscious work environment. (Radiation

Protection, Operations)

Example 2 - Employee Concerns Program Issues:

" The Employee Concerns Program does not maintain confidentiality. (Training)

" The Employee Concerns Program dismisses concerns without research. (Training)

  • Two workers would not raise issues to the Employee Concerns Program for fear of

retaliation. (Operations, Engineering)

  • The Employee Concerns Program was halted in the performance of an investigation.

(Maintenance)

Example 3 - Chilling Effects:

" A work environment where employees feel free to raise concerns does not exist within the

training and security departments, as well as the entire site in general. (Training, Security)

" A corrective action document was deleted from the corrective action program after the

plant manager chastised the originator for writing it. (Training)

" Workers do not feel comfortable raising issues to the NRC because several individuals who

have done so were terminated. (Radiation Protection)

Example 4 - The condition that caused damage to the residual heat removal pump suction relief

A3-1 Attachment 3

I C

valves has not been addressed in a timely manner. (Operations)

Example 5 - Callaway Plant was not recognizing and committing to doing the right thing with

regard to nuclear safety by not requesting a Technical Specification amendment that

restricted solid plant operations upon a loss of two cold overpressure mitigation

system relief. (Operations)

Evaluation - Examples 1, 2 and 3

The NRC provided in Ma 'nual Chapter 0305, "Operating Reactor Assessment Program," a

definition of a safety conscious work environment. Specifically, it is "an environment in which

employees feel free to raise safety concerns, both to their management and to the NRC, without

fear of retaliation and where such concerns are promptly reviewed, given their proper priority

based on their potential safety significance, and appropriately resolved with timely feedback to

employees."

Normally, an inspection team conducts 15 - 25 confidential intervie ws with employees to assess

the safety conscious work environment at plants during biennial problem identification and .

resolution inspections. To develop a comprehensive assessment of the safety conscious work

environment at Callaway Plant, the team interviewed 93 personnel in the operations, engineering,

maintenance, radiation protection, security, outage planning, radioactive waste management,

training, regulatory affairs and quality assurance organizations. The team used the questions

prescribed in Inspection Procedure 711 52B, "Identification and Resolution -of'Problems," to

determine employee attitudes regarding the safety conscious work environment at Callaway Plant.

The team informed the people selected by organizations who had expressed concern with the

safety conscious work environment and by the results of the Callaway Plant 2007 Safety Culture

Survey.

Generally, the team determined the following from the interviews:

" All personnel indicated that they would raise nuclear safety concerns by using one of the

four methods - corrective action program, supervisor, employee concerns program, or

NlRC. However, the team determined that not all individuals would use all of the methods

available to them. For example, one person indicated that he would not raise personal

issues unrelated to nuclear safety because he believed that management would take no

actions. Another individual indicated he would only talk to his supervisor.

" Not all employees would use the employee concerns program if they did not get

satisfaction from use of the corrective action program or from their supervisor. Specifically,

two individuals stated they did not trust the employee concerns program and would rather

talk to the NRC.

  • Thirty percent of the personnel interviewed had a misconception of the employee concerns

program (e.g., did not know the program coordinator had changed, did not know the

purpose of the employee concerns program, did not know the location of the coordinator's

office, et cetera)

A3-2 A3-2

Attachment 3

I . .

In addition, the team asked additional questions that reflected the statements of concerned

individuals. For 52 of the 93 interviews, the team member asked the following specific questions

to address the statements from concerned individuals in the operations, engineering, t~raining, and

radioactive waste management organizations:

  • Do you believe that you can readily disagree with your management?

" Does your management encourage differing views?

  • Does the culture here promote or inhibit using the corrective action program?.

" Is management open to hearing problems?

  • Is management reluctant to investigate problems fully?
  • Does management recognize and commit to doing the right thing with regard to nuclear

safety?

.The team interviewed workers, supervisors, and managers. The individuals interviewed had a

broad mix of experience at Callaway, from relatively new individuals to individuals with over

20 years of experience. The team questioned personnel on all of the operating crews. Without

exception, the personnel interviewed responded to the above additional questions that: they felt

free to disagree with all levels of management, the current culture at Callaway promotes effective

problem identification and resolution, management encourages employees to raise nuclear safety

problems and other concerns, and management fully investigates nuclear safety problems and

other concerns.

The licensee had performed several assessments of their safety conscious work environment that

included:

  • 2005 Synergy Safety Culture Survey
  • 2007 Synergy Safety Culture Survey
  • 2006 operations, engineering and training organization safety conscious work environment

surveys

  • 2008 Independent Assessment of Safety Conscious Work Environment At Callaway

Generally, these assessments and surveys identified that the licensee maintained a safety

conscious work environment; however, each of the surveys identified that general culture and work

environment factors needed attention. The external surveys identified on site organizations that.

had poor responses relative to industry norms and to other onsite organizations that responded to

the survey. Finally, each of the external surveys identified that the licensee should address the

general culture and work environment factors so that a safety conscious work environment issue

does not emerge. In response to the 2008 Independent Assessment, the licensee had initiated a

Significance Level 2 Callaway Action Request to determine the root cause(s) and develop

appropriate corrective actions. Since the licensee had not finalized'their cause evaluation and

A3-3 A3-3

Attachment 3

a I)

developed corrective actions at the time of this inspection, the next biennial problem identification

and resolution inspection will evaluate the effectiveness of the corrective actions.

Because of the consistent responses among these assessments and our interviews, the team

concluded that Callaway had maintained a safety conscious work environment although some

areas and organizations required additional oversight.

Evaluation - Example 4

Previously, NRC had reviewed the timeline for development and implementation of this

modification. NRC had concluded that the licensee did not properly develop the modification;

therefore, the licensee could not implement the modification during Refueling Outage 15. From

review of actions following the failure to implement the modification, NRC challenged the licensee

regarding the ability of the relief valve discharge line to perform its function. From discussions with

the licensee, NRC concluded that leaving the line unmodified would not significantly increase the

risk to the plant, that the licensee planned to implement the modification in a manner

commensurate with its safety significance and that the licensee had violated no regulations.

During this inspection, the team reviewed documentation related to implementing the modification

and related to the modification and corrective actions. The team interviewed personnel familiar

with implementation of the modification for the relief valves in the residual heat removal system.

The team verified that the licensee had completed and scheduled the modification identified as a

corrective action in Callaway Action Request 200601188. Modification Package 07-0007, "Modify

the RHR Suction Relief Discharge Piping."

Evaluation - Example 5

The team evaluated this technical concern related to depressurizing the reactor coolant system

while in solid plant conditions. The team performed the evaluation by interviewing plant personnel

and reviewing applicable documents that included: Technical Specifications and Technical

Specification Bases, Standard Technical Specifications, Technical Specification Task Force

documents, a license amendment request, and internal e-mails on this topic.

Technical Specification 3.4.12.G states that with two required relief valve inoperable, action shall

be taken to depressurize the reactor coolant system and establish a reactor coolant system vent

greater than 2.0 square inches within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Given this specification, it would appear that

depressurizing with saturated conditions (a steam bubble) in the pressurizer would allow better

pressure control than depressurizing with a solid pressurizer. Depressurizing with a steam bubble

would reduce the risk of overpressurization because of better pressure control.

The industry, through an owner's group initiative, proposed to increase the Technical Specification

completion time with an inoperable cold overpressure mitigation system from 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

for all three PWR designs. The NRC agreed this was a more realistic time to plan and execute the

evolution and endorsed it by revising necessary Standard Technical Specifications to allow.

a 12-hour completion time with an inoperable cold overpressure mitigation system. The licensee

submitted a license amendment request on November 29, 2007, which requests extending the

completion time from 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> to depressurize the reactor coolant system and establish

a vent.

A3-4 Attachment 3

C , I -

The license amendment did not request a limitation that the Technical Specification be carried out

exclusive of solid plant operations. Requesting such a limitation would exceed and be more

restrictive than what NRC had previously reviewed as acceptable for Technical Specification

changes. The licensee would have to demonstrate such a change as risk beneficial as described

in Regulatory Guide 1.200, "An Approach for Determining the Technical Adequacy of Probabilistic

Risk Assessment Results for Risk-Informed Activities."

The team determined through interviews and reviewing documented e-mails, discovered that

Callaway Plant personnel had discussed this issue with their industry Technical Specifications

group and submitted their licensee amendment request without a provision to prohibit solid plant

operation. This change to a 12-hour completion time would likely address the concern as

evidenced by a senior reactor operator at the Callaway Plant writing that the 12-hours allowed

should be enough to comply with the Technical Specification while the pressurizer remains

saturated With a steam bubble.

The team concluded that Callaway Plant management made an acceptable decision to not exceed

what was considered as an acceptable path to ensure plant safety by not prohibiting solid plant

operations with respect to Technical Specification 3.4.12.G. Further, based upon the discussions

in Examples 1, 2, and 3 above in general and based upon this instance specifically, the team

determined that Callaway Plant recognized and committed to take appropriate actions.

Specifically, the licensee researched the issue and submitted a Technical Specification

amendment that requested the longest completion time allowed by Standard Technical

Specifications.

A3-5 Attachment 3

I . -

Callaway Plant PI&R Inspection

Inspection Report 2008006

2/11 - 3/14/2008

G. Pick (4660)

PIM NRC NA NA NA March 14, 2008 71152B NA

Biennial Problem Identification & Resolution Assessment

The team reviewed 246 Callaway Action Requests, several job orders, engineering evaluations,

associated root and apparent cause evaluations, and other supporting documentation to assess

problem identification and resolution activities. The team reviewed an additional 124 Callaway

Action Requests related to specific areas - essential service water, component cooling

water, 480 Vac auxiliary contacts and safety conscious work environment. Based on the sample

selected for review, the team concluded the licensee continued to have challenges in the area of

prioritization and evaluation, which require additional effort. The team also noted that licensee

performance. related to problem identification and resolution had improved. The team determined

the licensee had used the self-assessment process and quality assurance organization to improve

site performance. The team determined the improvement resulted from corrective action process

improvements implemented in January 2007, and management oversight changes implemented

following receipt of substantive cross-cutting issue in problem identification and resolution.

The team determined that the licensee had initiated actions that improved the quality of their

operability assessments, operational decision-making, and knowledge of the detailed design and

licensing basis since the last evaluation. The graduated approach to assigning cause evaluations

for conditions adverse to quality and the change that required the Callaway Action Request

screening committee to review all Callaway Action Requests provided increased assurance in the

ability of the licensee to identify and effectively resolve conditions adverse to quality.

The team determined that the licensee properly evaluated industry operating experience when

performing root cause andhigher tier cause evaluations; however, the licensee had continued

challenges effectively evaluating industry operating experience.

The team determined that licensee audits and assessments continued to be detailed, probing, and

self-critical. The licensee continued to use benchmarking of industry best practices and third party

evaluations that improved the corrective action program performance during this assessment

period. The licensee had effectively implemented performance improvements to address the

substantive cross-cutting issue (refer to March 2, 2007, End of Cycle letter) related to .evaluating

actions required for conditions adverse to quality as demonstrated by the decreased number of

findings in the latter half of this assessment period and lower affect that poor evaluations had on

the facility. However, the licensee will need to apply additional effort to affect improvements. The

improving performance resulted from increased management involvement in the corrective action

program and in daily activities.

Because of the increased number of allegations at the facility in Calendar Year 2007, including

several discrimination concerns, the team interviewed more personnel than normal to assess the

safety conscious work environment at the Callaway Plant. The team documented the nature of the

concerns and the increased scope of the evaluations in Attachment 3. The team determined that

not all individuals were comfortable using all of the methods available to them for reporting

I " , -

concerns; however, all personnel would have used at least one of the methods available for

reporting a safety concern. In addition, the team determined that the employee concerns program

requires more visibility and that not all personnel had confidence in the employee concerns

program. The team determined that our review results remained consistent with other safety

culture surveys that Callaway Plant had completed within the last year. The team determined that

some general culture and work envir6nment issues continued to be present from the last

assessment that were outside NRC regulatory jurisdiction, which if not addressed could potentially

affect the safety conscious work environment at the Callaway Plant.

A. Inspector-Identified and Self-Revealing Findinqs

Cornerstone: Mitigating Systems

J. Groom (4660)

PIM NRC NCV BI Green March 14, 2008 71152B P.2(a)

Nonconservative Technical Specification for Battery Inter-cell Connection Resistances

The team identified a Green noncited violation of 10 CFR Part 50, Appendix B, Criterion Ill,

"Design Control," because the licensee failed to ensure that Technical Specification Surveillance

Requirements for the NK1 1 and NK14 safety-related batteries established limits that met the

design requirements. Specifically, until questioned by the team the licensee failed to determine

the required design value needed to assure plant safety as requested in Callaway Action

Request 200706561. The licensee determined that 69 micro-ohms should be the actual allowed

inter-cell voltage limit to meet the design requirements versus an allowed Technical Specification

limit of 150 micro-ohms.

The performance deficiency associated with this finding involved the failure to ensure that the

NK1 1 and NK14 safety-related batteries would remain operable if all the inter-cell connections

measured 150 micro-ohms as allowed by Technical Specification Surveillance

Requirements 3.8.4.2 and 3.8.4.5. This finding was greater than minor because it was

associated with the Mitigating Systems cornerstone attribute of maintenance and testing and

affects the associated cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using Manual

Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the finding was

determined to have very low safety significance because it was a design deficiency confirmed not

to result in loss of operability. The finding had a crosscutting aspect in the area of problem

identification and resolution associated with operating experience because the licensee failed to

evaluate in a timely manner relevant internal and external operating experience P.2(a).