ML042100540

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IR 05000313-04-003, 05000368-04-003, on 03/25/2004 - 06/23/2004; Arkansas Nuclear One, Units 1 and 2; Equip. Align., Fire Prot., Maint. Risk Assess., Op. Eval., Perm. Plant Mods., Out. Act., Access Control, Event Followup, Other Activities
ML042100540
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 07/27/2004
From: Troy Pruett
NRC/RGN-IV/DRP/RPB-D
To: Forbes J
Entergy Operations
References
IR-04-003
Download: ML042100540 (51)


See also: IR 05000313/2004003

Text

July 27, 2004

Jeffrey S. Forbes, Vice President,

Operations

Arkansas Nuclear One

Entergy Operations, Inc.

1448 S.R. 333

Russellville, Arkansas 72801-0967

SUBJECT: ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT

05000313/2004003 and 05000368/2004003

Dear Mr. Forbes:

On June 23, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Arkansas Nuclear One, Units 1 and 2, facility. The enclosed integrated report documents

the inspection findings, which were discussed on June 30, 2004, with Mr. C. Eubanks and other

members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

This report documents nine NRC identified and self-revealing findings of very low safety

significance (Green). Eight of these findings were determined to involve violations of NRC

requirements; however, because of the very low safety significance and because they were

entered into your corrective action program, the NRC is treating these findings as noncited

violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. Additionally, a

licensee-identified violation, which was determined to be of very low safety significance, is listed

in Section 4OA7 of this report. If you contest these noncited violations, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington

DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory

Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington

DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One, Units 1 and 2,

facility.

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

Entergy Operations, Inc. -2-

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Troy W. Pruett, Chief

Project Branch D

Division of Reactor Projects

Dockets: 50-313

50-368

Licenses: DPR-51

NPF-6

Enclosure:

NRC Inspection Report 05000313/2004003 and 05000368/2004003

w/Attachment: Supplement Information

cc w/enclosure:

Senior Vice President

& Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Manager, Washington Nuclear Operations

ABB Combustion Engineering Nuclear

Power

12300 Twinbrook Parkway, Suite 330

Rockville, MD 20852

County Judge of Pope County

Pope County Courthouse

100 West Main Street

Russellville, AR 72801

Entergy Operations, Inc. -3-

Winston & Strawn

1400 L Street, N.W.

Washington, DC 20005-3502

Bernard Bevill

Radiation Control Team Leader

Division of Radiation Control and

Emergency Management

Arkansas Department of Health

4815 West Markham Street, Mail Slot 30

Little Rock, AR 72205-3867

James Mallay

Director, Regulatory Affairs

Framatome ANP

3815 Old Forest Road

Lynchburg, VA 24501

Entergy Operations, Inc. -4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

Senior Resident Inspector (RWD)

Branch Chief, DRP/D (TWP)

Acting Senior Project Engineer, DRP/D (CJP)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (KEG)

Jennifer Dixon-Herrity, OEDO RIV Coordinator (JLD)

ANO Site Secretary (VLH)

ADAMS: * Yes * No Initials: ______

  • Publicly Available * Non-Publicly Available * Sensitive * Non-Sensitive

R:\_ANO\2004\AN2004-03RP-RWD.wpd

RIV:RI:DRP/D RI:DRP/D SRI:DRP/D PE:DRP/D SPE:DRP/D

JLDixon ELCrowe RWDeese DEDumbacher CJPaulk

T to TWPruett T to TWPruett T to TWPruett TWPruett for /RA/

7/19/04 7/19/04 7/19/04 7/18/04 7/21/04

C:DRS/PSB C:DRS/EB C:DRS/OB C:DRS/PEB C:DRP/D

MPShannon JAClark ATGody LJSmith TWPruett

/RA/ /RA/ GEWerner for RPMullkin for /RA/

7/25/04 7/22/04 7/23/04 7/23/04 7/27/04

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-313, 50-368

Licenses: DPR-51, NPF-6

Report: 05000313/2004003 and 05000368/2004003

Licensee: Entergy Operations, Inc.

Facility: Arkansas Nuclear One, Units 1 and 2

Location: Junction of Hwy. 64W and Hwy. 333 South

Russellville, Arkansas

Dates: March 25 through June 23, 2004

Inspectors: J. Clark, Engineering Branch Chief

E. Crowe, Resident Inspector

R. Deese, Senior Resident Inspector

J. Dixon, Resident Inspector

D. Dumbacher, Project Engineer

G. George, Reactor Inspector

R. Lantz, Sr. Emergency Preparedness Inspector

C. Paulk, Senior Project Engineer

L. Ricketson, P.E., Senior Health Physicist

Approved By: Troy W. Pruett, Chief, Project Branch D

Division of Reactor Projects

Enclosure

CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R12 Maintenance Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . . 8

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R16 Operator Work-Arounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . 19

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

2OS1 Access Control To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 20

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA1 PI Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA4 Cross Cutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

40A7 Licensee-identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

ATTACHMENT: SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7

Enclosure

SUMMARY OF FINDINGS

IR 05000313/2004003, 05000368/2004003; 03/25/04 - 06/23/04; Arkansas Nuclear One,

Units 1 and 2; Equip. Align., Fire Prot., Maint. Risk Assess., Op. Eval., Perm. Plant Mods., Out.

Act., Access Control, Event Followup, Other Activities.

This report covered a 3-month period of inspection by resident and regional inspectors.

Eight Green noncited violations and one Green finding were identified. The significance of

most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, "Significance Determination Process." Findings for which the significance

determination process does not apply may be Green or be assigned a severity level after NRC

management's review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3,

dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. A self revealing finding was reviewed for the inadequate identification

and resolution of problems with the main turbine trip oil system that contributed

to a turbine trip and reactor trip on Unit 1. Because the licensee did not

adequately address problems with operation of the main turbine lube oil system,

an operator released the main turbine reset lever after mistakenly thinking a

main turbine trip had been reset. Corrective actions taken or planned by the

licensee have been entered into the licensee's corrective action program. This

issue involved human performance cross-cutting aspects associated with

operations personnel not fully informing all members of the on-shift crew of plant

conditions.

The finding is greater than minor because it was analogous to Example 4.d in

Appendix E, "Examples of Minor Issues," of Manual Chapter 0612, "Power

Reactor Inspection Reports," because the failure to take adequate corrective

action contributed to an operator error. Using the Phase 1 worksheet in Manual

Chapter 0609, "Significance Determination Process," the finding was determined

to have very low safety significance because, although it resulted in a reactor

trip, no other complicating events were caused by the error and all mitigating

systems remained available to the operators (Section 4OA3).

Cornerstone: Mitigating Systems

Appendix B, Criterion XVI, for the failure to correct inaccurate main control room

valve position indicators on the Unit 2 high and low pressure safety injection

system motor-operated valves. The valve position indicators were not calibrated

for approximately 8 years yet were relied upon for indication in station

procedures, including the loss of shutdown cooling procedure. Corrective

Enclosure

-2-

actions taken or planned by the licensee have been entered into the licensees

corrective action program. This issue involved problem identification and

resolution cross-cutting aspects associated with operations personnel not

identifying conditions adverse to quality.

The finding is greater than minor because it affected the mitigating systems

cornerstone objective of ensuring the reliability of systems that respond to

initiating events to prevent undesirable consequences. Using the Phase 1

worksheets in Manual Chapter 0609, "Significance Determination Process," the

finding was determined to have very low safety significance because the safety

function of the valves was not affected and other indications were available to

monitor system performance (Section 1R04).

  • Green. The inspectors identified a noncited violation of Unit 1 Technical

Specification 5.4.1.c and Unit 2 Technical Specification 6.8.1.f when the licensee

provided inadequate manual suppression firefighting equipment upon a loss of

automatic and manual suppression to the intake structures and service water

pump areas. The equipment staged by the licensee would have required

numerous actions by the fire brigade to ready a fire hose for manual fire

suppression. Corrective actions taken or planned by the licensee have been

entered into the licensee's corrective action program. This issue involved human

performance cross-cutting aspects associated with operations personnel not

implementing appropriate compensatory measures.

The finding is greater than minor because it affected the mitigating systems

cornerstone objective of ensuring the availability of systems that respond to

initiating events to prevent undesirable consequences. Using Appendix F,

"Determining Potential Risk Significance of Fire Protection and Post-Fire Safe

Shutdown Inspection Findings," of Manual Chapter 0609, "Significance

Determination Process," the finding was determined to have very low safety

significance because all remaining mitigating systems needed to respond to a

loss of service water on either unit were available (Section 1R05).

the failure to perform adequate risk assessments on Units 1 and 2. The licensee

failed to update a prior risk assessment due to changing external events

(declaration of a tornado watch) that could have had an impact on the existing

assessment (increased likelihood of grid instability). In addition, the licensee did

not include the added external risk from fire and its impact on safe shutdown

equipment in aggregate risk assessments for the plant. Corrective actions taken

or planned by the licensee have been entered into the licensee's corrective

action program.

The inspectors determined that these issues are more than minor because, if left

uncorrected, they would become a more significant safety concern in that future

risk assessments could result in failures to properly manage increases in risk.

Using the Phase 1 worksheets in Manual Chapter 0609, "Significance

Enclosure

-3-

Determination Process," the finding was determined to have very low safety

significance because mitigating systems were available and it did not affect the

likelihood of external initiating events (Section 1R13).

Appendix B, Criterion XVI, for the failure to take timely corrective action to

correct indications of material wastage on Unit 2 Containment Spray Pump B.

Specifically, the licensee did not implement actions to remove discolored boric

acid deposits from the containment spray pump for approximately 9 months.

Corrective actions taken or planned by the licensee have been entered into the

licensee's corrective action program. This issue involved problem identification

and resolution cross-cutting aspects associated with the timely implementation of

corrective actions for conditions adverse to quality.

The inspectors determined that this issue is more than minor because if left

uncorrected it could become a more significant safety concern in that continued

wastage of the pump could impact operability. Using the Phase 1 worksheets in

Manual Chanter 0609, "Significance Determination Process," the finding was

determined to have very low safety significance because the actual wastage of

the pump studs, nuts, and washers did not affect the safety function of the

containment spray pump (Section 1R15).

  • Green. The inspectors identified a noncited violation of Unit 1 Technical

Specification 5.4.1.a for the failure to follow procedures for equipment control.

The licensee failed to follow Procedure OP-102, "Protective Tagging,"

Revision 1, in several respects in their use of "Do Not Operate" tags on

motor-operated valve handwheels prior to the Unit 1 refueling outage.

These failures are greater than minor in that they affected the mitigating systems

cornerstone attribute of equipment availability. Using the Phase 1 worksheets in

Manual Chapter 0609, "Significance Determination Process," the finding was

determined to have very low safety significance because the tagging process did

not affect any automatic safety functions (Section 1R20).

Cornerstone: Barrier Integrity

  • Green. The inspectors identified a noncited violation of Unit 1 Technical

Specification 5.4.1.a for the failure to follow written procedures associated with

the inspection of the reactor vessel bottom nozzle penetrations during Refueling

Outage 1R18. Specifically, the licensee failed to inspect 100 percent of the

lower head penetrations during inspections required by Procedure 2311.09, "Unit

1 and Unit 2 Alloy 600 Inspection," Revision 5 as described in NRC Bulletin

2003-002. Corrective actions taken or planned by the licensee have been

entered into the licensee's corrective action program. This issue involved human

performance cross-cutting aspects associated with inattention to detail by

engineering personnel during inservice examinations.

Enclosure

-4-

This finding is greater than minor because it affected the reactor safety barrier

integrity cornerstone objective for providing reasonable assurance that physical

design barriers protect the public from radionuclide releases caused by accidents

or events. Using the Phase 1 worksheets in Manual Chapter 0609, "Significance

Determination Process," the finding was determined to have very low safety

significance because no actual leakage from the reactor vessel penetrations

occurred (Section 4OA5).

Cornerstone: Occupational Radiation Safety

  • Green. The inspector identified an event in which the licensee failed to control a

high radiation area in violation of Unit 2 Technical Specification 6.13.1 after

workers received abnormal dosimeter readings on October 14, 2003. The

licensee performed dose measurements and found an uncontrolled high

radiation area in the Unit 2 sample cooler room. The licensee should have been

alerted to the potential for a high radiation area in this room when reactor coolant

system radioactivity levels increased and high radiation areas were identified in

adjoining areas on October 12, 2003. Corrective actions taken or planned by the

licensee have been entered into the licensee's corrective action program. The

issue involved human performance cross-cutting aspects associated with the

thoroughness of radiation surveys by radiation protection personnel.

The failure to control a high radiation area is a performance deficiency. This

finding is greater than minor because it was associated with one of the

cornerstone attributes and affected the cornerstone objective, in that, inadequate

exposure controls of a high radiation area affected the licensees ability to

ensure adequate protection of worker health and safety from exposure to

radiation. Because the finding involved the potential for workers to receive

significant, unplanned, unintended dose as a result of conditions contrary to

Technical Specification requirements, the inspector used the occupational

radiation safety significance determination process described in Manual

Chapter 0609, "Significance Determination Process," Appendix C, "Occupational

Radiation Safety Significance Determination Process," to analyze the

significance of the finding. The inspector determined that the finding was of very

low safety significance because it did not involve (1) ALARA planning and

controls, (2) an overexposure, (3) a substantial potential for overexposure, or

(4) an impaired ability to assess dose (Section 2OS1).

Cornerstone: Public Radiation Safety

  • Green. A self revealing noncited violation of Unit 2 Technical

Specification 6.8.1.a was reviewed for the failure to follow written procedures

associated with the modification of the reactor coolant sample sink. Specifically,

the licensee improperly connected the discharge of the reactor coolant sample

sink into a secondary drain header which ultimately drained into the main

condenser. Corrective actions taken or planned by the licensee have been

entered into the licensee's corrective action program.

Enclosure

-5-

This finding is more than minor because it was analogous to Example 3.a in

Appendix E, "Examples of Minor Issues," of Manual Chapter 0612, "Power

Reactor Inspection Reports," because the modification required rework to

correctly address design concerns. Using Appendix D, "Public Radiation Safety

Significance Determination Process," of Manual Chapter 0609, "Significance

Determination Process," the finding was determined to have very low safety

significance because the licensee was able to assess the amount and curie

content of the reactor coolant introduced into the secondary plant and there was

no dose impact to the public (Section 1R17).

B. Licensee-Identified Violations

A violation of very low safety significance which was identified by the licensee has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and its

corrective actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent rated thermal power and remained there until

April 20, 2004, when the unit was shut down for Refueling Outage 1R18. The unit was

restarted on May 12 and resumed 100 percent power operation on May 16. The unit remained

at or near 100 percent power until June 11 when the unit was shut down to repair an internal

leak on the main turbine. The unit was restarted on June 19 and resumed 100 percent power

operation on June 20. The unit remained at or near 100 percent power for the remainder of the

inspection period.

Unit 2 began the inspection period at 100 percent rated thermal power and remained there

throughout the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

a. Inspection Scope

During the week of June 7, 2004, the inspectors reviewed the actions taken by the

licensee to prepare for tornadoes, specifically looking at precautions and design

features to ensure the operability, functionality, and availability of the Q condensate

storage tank (QCST). The inspectors performed a walkdown of the QCST and its

surroundings to verify prescribed measures were taken to ensure an adequate water

inventory would be available to the emergency feedwater systems in the event of a

tornado. Finally, the inspectors reviewed Calculations 82-D-2086-01, "Volume of

Condensate Storage Tank T41-B Requiring Tornado Missile Protection," Revision 2,

and 97-E-0010-01, "Emergency Feedwater Pump Suction Low Pressure Alarm,"

Revision 0, to verify adequate tornado missile coverage of the QCST.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

a. Inspection Scope

Partial System Walkdowns. The inspectors performed three partial system walkdowns

of systems important to reactor safety during this inspection period in order to verify the

operability of the systems. The inspectors reviewed system operating instructions and

required system valve and breaker lineups and then compared them to operator logs,

control room indications, valve positions, breaker positions, and control circuit

indications to verify these components were in their required configuration for making

Enclosure

-2-

the systems operable. The inspectors also examined component material condition.

The following walkdowns were conducted:

  • On April 27, 2004, the inspectors performed a partial system walkdown of

accessible portions of Unit 1 Emergency Diesel Generator (EDG) K-4A and its

support systems during a refueling outage when the Unit 1 EDG K-4B was

inoperable due to maintenance.

  • On June 2, 2004, the inspectors performed a partial system walkdown of the red

train of the Unit 1 reactor building spray system when the green train of the

reactor building spray was removed from service during maintenance on Reactor

Building Spray Pump P-35B.

  • During the week of June 7, 2004, the inspectors performed a partial system

walkdown of the green train of the Unit 2 high pressure safety injection

system (HPSI) during the installation and testing of the temporary HPSI

pressurization system. The walk-down included the temporary HPSI

pressurization system.

b. Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, for the licensee's failure to correct inaccurate main control

room valve position indicators on the Unit 2 HPSI and low pressure safety

injection (LPSI) motor-operated valves (MOVs).

Description. During a control room walkdown in Unit 2, inspectors noted that the HPSI

and LPSI injection MOVs had remote position indicators, commonly called z-tape

indicators, adjacent to their valve operating switches which indicate the percentage the

valves are opened. The valves, which allow flow to the reactor coolant system loops,

were in their normally closed positions. The inspectors noted that while the valve

position indication lights for the MOVs indicated that the valves were closed, the z-tape

indicators showed various positions other than the actual position of the valves.

When the inspectors questioned the operators as to the true position of the valves, the

operators responded that the indicators were not accurate. The inspectors discovered

that the indicators had been out of calibration for approximately 8 years. A review of

operating procedures by inspectors demonstrated that, in numerous instances, control

room operators were directed to open the valves to 10 percent. Most of the operations

were just to bleed off system pressure, but for the LPSI MOV's, opening the valves

provided a flow path to prevent pump damage to the LPSI pumps. Licensee operators

indicated that they would accomplish this step by use of the z-tape indicators. The

inspectors determined that operations personnel could not rely upon the z-tape

indicators alone to prevent pump damage.

The inspectors could not find, nor could the licensee produce: (1) any open work orders

to calibrate the indicators, (2) condition reports (CRs) to address the deficiency, or

Enclosure

-3-

(3) any procedure changes to discontinue use of the indicators. As a result, the

inspectors concluded that the licensee had not adequately addressed the deficiency in

their corrective action program processes.

Analysis. The inspectors determined that this finding is greater than minor because it

affected the mitigating systems cornerstone objective of ensuring the reliability of

systems that respond to initiating events to prevent undesirable consequences. Using

the Phase 1 worksheets in Manual Chapter 0609, "Significance Determination Process,"

the finding was determined to have very low safety significance (Green) because the

safety function of the HPSI and LPSI valves were not affected and other indications

were available to monitor system performance. This issue involved problem

identification and resolution cross-cutting aspects associated with operations personnel

not identifying conditions adverse to quality.

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, requires that measures be

established to correct conditions adverse to quality. Contrary to the above, licensee

personnel did not identify or correct a condition adverse to quality involving errant valve

position indicators on the Unit 2 HPSI and LPSI injection MOVs. Because of the very

low safety significance and because the licensee included this condition in their

corrective action program as CR ANO-2-2004-0840, this violation is being treated as a

noncited violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000368/2004003-01, Failure to Correct Inaccurate HPSI and LPSI Valve

Position Indications.

1R05 Fire Protection (71111.05)

a. Inspection Scope

Routine Inspection

The inspectors referenced the Fire Hazards Analysis Report, Revision 8, during the

following inspections of seven fire areas to ensure that conditions were consistent with

the requirements of the licensees fire protection program for system design, control of

transient combustibles and ignition sources, fire detection and suppression capability,

fire barriers, and any related compensatory measures:

  • Fire Zone 144-D, Unit 1 upper south electrical penetration room on April 6, 2004
  • Fire Zone 20-Y, Unit 1 radwaste processing room on April 9, 2004
  • Fire Area N, Unit 1 intake structure on May 4, 2004
  • Fire Area OO, Unit 2 intake structure on May 4, 2004
  • Fire Zone 2024-JJ, Unit 2 emergency feedwater pump room (turbine driven) on

May 18, 2004

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  • Fire Zone 2025-JJ, Unit 2 emergency feedwater pump room, on June 2, 2004
  • Fire Zone 167-B, Unit 1 computer transformer room, on June 4, 2004

b. Findings

Introduction. The inspectors identified a Green NCV of Unit 1 Technical

Specification 5.4.1.c and Unit 2 Technical Specification 6.8.1.f when the licensee

provided inadequate compensatory fire fighting equipment in response to a loss of

manual and automatic suppression to the Unit 1 and 2 intake structures.

Description. On May 1, 2004, the licensee discovered a leak in the site fire water

header. Upon isolating the leak, the licensee isolated the fire water supply to the intake

structures for Units 1 and 2. This action secured the water supply to the fire fighting

hose reel in the Unit 1 intake structure and the automatic fire suppression systems for

both intake structures, thus rendering all manual and automatic firefighting systems

inoperable.

The licensee posted fire watches as a compensatory action for degraded fire fighting

features as required by Procedure 1000.152, "Unit 1 & 2 Fire Protection System

Specifications," Revision 3. This procedure required routing of an additional equivalent

capacity fire hose from an operable hose station.

On May 4, 2004, the inspectors walked down the compensatory fire hose and noted

several deficiencies. First, the large fire hose was not readily connectable to a usable

fire hose. In the event of an intake structure fire, the fire brigade would have to retrieve

a Y-connector from a hose house in order to hook up a standard fire hose. Second, the

inspectors noted that the fire brigade would have to break the existing Hose Reel 57

connection and hook it up to the large fire hose with the freshly retrieved Y-connector.

Finally, the inspectors noted that the fire brigade would have to connect the large fire

hose to the hydrant and unroll the large fire hose across the maintenance access road

and connect it to the hose leading to the intake structure. The inspectors considered

this compensatory fire hose layout to be inadequate, and therefore, concluded that the

licensee did not meet the requirements of the fire protection program.

Analysis. The inspectors determined that this finding was greater than minor because it

affected the mitigating systems cornerstone objective of ensuring the availability of

systems that respond to initiating events to prevent undesirable consequences. Using

Appendix F, "Determining Potential Safety Significance of Fire Protection and Post-Fire

Safe Shutdown Inspection Findings," of Manual Chapter 0609, "Significance

Determination Process," the inspectors evaluated a fire scenario in each intake structure

which caused a loss of service water on that unit assuming that manual suppression and

automatic suppression were highly degraded. The inspectors used the ignition

frequencies from the licensee's internal plant examination for external events, combined

with the remaining mitigation capability determined from the significance determination

process Phase 2 notebooks for the loss of service water scenarios on Units 1 and 2.

The inspectors determined that this issue was of very low safety significance (Green)

Enclosure

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because of the availability of mitigating systems and the short duration of the condition.

This issue involved human performance cross-cutting aspects associated with

operations personnel not following procedures and not implementing appropriate

compensatory measures.

Enforcement. Unit 1 Technical Specification 5.4.1.c, "Fire Protection Program

Implementation," and Unit 2 Technical Specification 6.8.1.f, "Fire Protection Program

Implementation," required establishing back-up fire suppression equipment upon a loss

of normal fire suppression equipment to the intake structures. Contrary to the above,

during the period of May 1-4, 2004, the licensee failed to provide adequate back-up fire

suppression equipment upon a loss of fire suppression equipment at the intake

structures. Because of the very low safety significance and because the licensee

included this condition in their corrective action program as CR ANO-C-2004-0828, this

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000313/2004003-02; 05000368/2004003-02, Failure to

Provide Adequate Compensatory Measures for a Loss of Fire Water to the Intake

Structure.

1R08 Inservice Inspection Activities (71111.08)

1. Inspection Scope

a. Performance of Nondestructive Examination Activities Other than Steam Generator

Tube Inspections

Inspection Procedure 71111.08 specifies that a minimum of two examinations be

reviewed, either through direct observation or by record review. The inspector

completed review of three examinations (one ultrasonic, one liquid penetrant, and one

radiographic). The inspector observed the ultrasonic and liquid penetrant examinations

and reviewed the records for the radiographic examination, all listed in the attachment

under Section 1R08.

During the observation of the ultrasonic and liquid penetrant examinations, the inspector

verified that the examiners used the correct nondestructive examination procedure, met

the requirements specified in the procedure, and used properly calibrated test

instrumentation and equipment. The inspector verified the certifications of the

individuals observed performing the examination. The inspector also reviewed the

radiographic procedure and certifications of the radiographer and the Level III reviewer.

The inspection procedure also specifies a review of examinations from the previous

outage with recordable indications that were accepted for continued service. There

were no recordable indications accepted for continued service.

The inspection procedure further specifies that, if welding had been completed on the

pressure boundary for the American Society of Mechanical Engineer (ASME) Code

Class 1 or 2 systems, then the inspector should verify that acceptance and preservice

examinations were done in accordance with the ASME Code for at least one weld. The

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inspection procedure also specifies that verification of at least one ASME Code,

Section XI repair or replacement meet ASME Code requirements. The inspector

reviewed the four weld packages listed in the attachment under Section 1R08. Included

in these packages were two welds performed as repair activities.

b. Steam Generator Tube Inspection Activities

Section 03.02 of the procedure requires, at a minimum, the completion of steps 02.04a.,

c., d., g.(1), h., i., and j. for all steam generator tube inspections. In addition, because

the steam generator tubes are made of mill annealed Inconel Alloy 600 steel, the

remainder of Section 02.04 is also required to be performed. The inspector reviewed

the in-situ testing criteria, compared the estimated number and size of flaws to the

actual numbers, reviewed the scope and expansion criteria for eddy current testing,

verified that all areas of potential degradation were examined, confirmed that the repair

methods and criteria were approved, and verified that the probes and equipment were

qualified. As a result, the inspector performed all of the required inspection activities

with the following exceptions:

Section 02.02a.3. was not performed because all in-situ testing

had been completed,

Section 02.02d. was not performed because no new degradation

mechanisms were identified,

Section 02.02h. was not performed because the leakage was less

than 3 gallons per day, and

Section 02.02j. was not performed because no loose parts or

foreign material was identified.

c. Identification and Resolution of Problems

The inspector reviewed four CRs issued since the last outage on inservice inspection

and steam generator eddy current testing activities. The inspector verified that licensee

personnel identified, evaluated, corrected, and trended inservice inspection problems.

2. Findings

No findings of significance were identified.

Enclosure

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1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

The inspectors observed one session of licensed operator requalification training

activities in the Unit 2 simulator to assess the licensees effectiveness in conducting the

requalification program and to verify that licensed individuals received the appropriate

level of training required to maintain their licenses.

  • On June 17, 2004, the inspectors observed the Unit 2 licensed operator

simulator qualification training Scenario A2SPGLOR040401, "Fire or Explosion,"

conducted for Training Cycle 4.

The inspectors compared their observations for this scenario to the applicable abnormal

operating procedures, emergency plan procedures, and applicable Technical

Specifications. In addition, the inspectors attended the critique following the scenario

held by the Unit 2 training organization.

b. Findings

No findings of significance were identified.

1R12 Maintenance Implementation (71111.12)

a. Inspection Scope

The inspectors reviewed a performance problem associated with failures of the Unit 1

main steam safety valves to lift within tolerance in order to assess the effectiveness of

the Maintenance Rule Program. The inspectors independently verified that licensee

personnel properly implemented 10 CFR 50.65, "Requirements for Monitoring the

Effectiveness of Maintenance at Nuclear Power Plants."

The inspectors focused the review on whether the structures, systems, or components

(SSCs) that experienced problems were properly characterized in the scope of the

program. They also reviewed whether the SSC failure or performance problem was

properly characterized. The inspectors assessed the adequacy of the licensee's

significance classification for the SSC. This included the appropriateness of the

performance criteria established for the SSC and the adequacy of corrective actions for

SSCs classified in accordance with 10 CFR 50.65 (a)(1).

b. Findings

No findings of significance were identified.

Enclosure

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1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a. Inspection Scope

The inspectors evaluated and discussed with the licensee the six risk assessments

listed below to verify that they were performed when required. The inspectors reviewed

these assessed risk configurations against actual plant conditions and in-progress

evolutions or external events to verify that the assessments were accurate, complete,

and appropriate for the conditions. In addition, the inspectors walked down the control

room and plant areas to verify that compensatory measures identified by the risk

assessments were appropriately performed.

  • Planned maintenance on the Unit 2 Service Water Pump C during the week of

March 1, 2004

  • Planned maintenance on the Unit 1 Door 48, the south switchgear room/turbine

building door, from April 12-14, 2004

  • Daily review of risk assessments during Refueling Outage 1R18 completed in

accordance with ANO Shutdown Operations Protection Plan dated

January 16, 2004, and comparison to actual plant conditions to ensure that the

licensee implemented acceptable defense-in-depth strategies for critical safety

functions

  • Planned maintenance and severe weather affecting Unit 2 during the week of

April 26, 2004

  • Maintenance on Unit 2 during the week of May 10, 2004
  • Maintenance on Unit 1 during the week of May 17, 2004

b. Findings

Introduction. The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the

failure to perform an adequate risk assessment due to emergent external conditions and

found previous instances where the licensee failed to adequately consider external

events.

Description. The licensee failed to update a prior risk assessment due to changing

external environmental conditions. During the week of March 1, 2004, the licensee

performed maintenance on the Unit 2 Service Water Pump C, 2P-4C. During the

maintenance period, the National Weather Service issued a tornado watch. The

inspectors questioned licensee personnel on how the tornado watch impacted their risk

assessment for the unit. The inspectors determined that the licensee had not

reassessed risk for weather conditions which had an imminent or high probability of

occurrence. Also, the inspectors discovered that the licensees Common Operations

Directive COPD-024, Risk Assessment Guidelines, Revision 9, along with both units'

Enclosure

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procedures for natural emergencies, Procedures OP 1203.025, "Natural Emergencies,"

Revision 19, and OP 2203.008, "Natural Emergencies," Revision 8, did not contain

instructions to re-evaluate risk based on changing external conditions (e.g., adverse

weather). The Risk Assessment Guidelines directive is the document the licensee uses

to implement 10 CFR 50.65(a)(4). The Natural Emergencies procedures are the

procedures that would trigger the operators to re-evaluate plant risk for the changing

external conditions, using the Risk Assessment Guidelines. From this, the inspectors

concluded that the licensee did not have in place a method to re-evaluate plant risk for

either unit based on changing external conditions and, as a result, did not adequately

reassess risk due to this emerging condition.

The inspectors also found that the licensee failed to consider the external risk from fire

and its impact on safe shutdown equipment in previous risk assessments. The

emergency feedwater pumps, EDGs, and high pressure and low pressure safety

injection systems are important safety significant systems needed to achieve and

maintain safe shutdown conditions following a fire event (switchgear fire, main control

room fire, etc.). The licensee had not evaluated the removal of these systems from

service; even though, they are needed to mitigate identified risk from fire initiating

events. Consequently, additional actions to manage the increased risk were not

considered. The inspectors reviewed COPD-024, "Risk Assessment Guidelines,"

Revision 9, and determined that no provisions were made in the licensees process to

account for known risk contributors.

Analysis. The inspectors determined that these issues were more than minor because if

left uncorrected they would become a more significant safety concern in that actions to

manage increases in risk may not be implemented. Using the Phase 1 worksheets in

Manual Chapter 0609, "Significance Determination Process," the finding was

determined to have very low safety significance (Green) because mitigating systems

were available and it did not affect the likelihood of an external initiating event.

Enforcement. 10 CFR 50.65(a)(4) requires, in part, that the licensee shall assess and

manage the increase in risk that may result from the proposed maintenance activities.

Contrary to this, the licensee did not adequately assess risk based on external events.

Because of the very low safety significance and because the licensee included this

condition in the corrective action program as CRs ANO-C-2004-0548 and -0982, this

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000313/2004003-03; 05000368/2004003-03, Failure to

Adequately Assess Risk Due to External Conditions.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the five operability determinations listed below to assess the

evaluations, the use of compensatory measures, and compliance with the Technical

Specifications. The inspectors review included a verification that operability

determinations were made as specified by the licensees Procedure LI-102, "Corrective

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Action Process," Revision 2, and Procedure 1015.047, "Condition Reporting Operability

and Immediate Reportability Determinations," Revision 0. The technical adequacy of

the determinations was reviewed and compared to the Technical Specifications, the

Technical Requirements Manual, the Updated Final Safety Analysis Report, and the

associated licensing-basis documentation.

  • Unit 2 HPSI voiding in the green train header, primarily around the injection valve

for the Safety Injection Tank A 2CV-5016-2

Room Exhaust Fan VEF-34, Hydrogen Purge Supply Isolation MOV CV-7444,

and Decay Heat Removal Unit Cooler VUC-1D

  • Accumulation of discolored boric acid deposits on studs, nuts, and washers for

the Unit 2 Containment Spray Pump 2P-35B motor mounts

  • Unit 1 Room 170 environmental qualification for electrical equipment essential to

the operation of the turbine-driven emergency feedwater pump

Room Cooler E-35B did not meet design service water flows during as-found

service water flow test done in Refueling Outage 1R18

b. Findings

Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion XVI, for the failure to promptly clean discolored boric acid deposits on Unit 2

Containment Spray Pump B.

Description. On February 15, 2004, operations personnel noted discolored boric acid

deposits on three of the Unit 2 Containment Spray Pump B studs and initiated

CR ANO-2-2004-0292. This CR documented the fact that boric acid deposits had been

a recurring issue on this pump as documented in CR ANO-2-2003-0674 initiated

May 9, 2003. The inspectors independently discovered the same condition on

February 24, 2004. The inspectors questioned licensee personnel to determine why the

boric acid deposits had not been cleaned and evaluated. Licensee personnel informed

the inspectors that they could not find any records associated with the removal of boric

acid from the pump and that they would address removal of the deposits on the pump.

In a follow-up tour of the pump area on March 24, 2004, the inspectors noted that the

boric acid deposits were still present on the pump. The inspectors noted that the

deposits had existed for approximately nine months with indications of material wastage

(discolored boric acid) and no apparent action by the licensee to remove the boric acid.

Licensee personnel informed the inspectors that removal of the deposits would occur

during an inspection of the pump in July 2004. The inspectors considered this action to

be untimely due to the indications of active material wastage. Additionally, the

Enclosure

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inspectors determined that Procedure 1032.037A, "Identification and Evaluation of Boric

Acid Leakage," did not provide guidance for correcting conditions where boric acid was

corroding material. The licensee, subsequently, cleaned the deposits on

March 26, 2004. A picture of the pump before cleaning is included in the attachment.

Analysis. The inspectors determined that the issue was greater than minor because if

left uncorrected it would become a more significant safety concern in that continued

wastage could impact the integrity of the pump. Using the Phase 1 worksheets in

Manual Chapter 0609, "Significance Determination Process," the inspectors determined

that the finding had very low safety significance (Green) because the containment spray

pump remained functional. This issue involved problem identification and resolution

cross-cutting aspects associated with the timely implementation of corrective actions for

conditions adverse to quality.

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, states, in part, that measures

shall be established to assure that conditions adverse to quality are promptly identified

and corrected. Contrary to the above, the licensee did not promptly correct a condition

adverse to quality involving material wastage on the Unit 2 containment spray pump.

Because of the very low safety significance and because the licensee included this

condition in their corrective action program as CR ANO-2-2004-0620, this violation is

being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000368/2004003-04, Untimely Corrective Action to Clean Discolored Boric Acid

Deposits.

1R16 Operator Work-Arounds (71111.16)

a. Inspection Scope

Semiannual Review. The inspectors sampled three attributes in a semi-annual review of

all operator workarounds listed on the licensees operator work-around list for both

Units 1 and 2. The cumulative effects of all workarounds on each unit were reviewed

for: (1) the reliability, availability, and potential for misoperation of a system, (2)

potential affects on multiple mitigating systems, and (3) the ability of operators to

respond to plant transients or accidents in a correct and timely manner.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)

a. Inspection Scope

Annual Review. The inspectors reviewed the licensees modification to the Unit 2

reactor coolant sample sink. The modification involved the use of a hydrogen/oxygen

analyzer and the use of a pH/conductivity analyzer for online sampling of the reactor

coolant system. The inspectors review assessed the controls related to the modification

Enclosure

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of the Unit 2 primary sample sink, which resulted in connecting the reactor coolant

system sample piping to a drain header that communicates with secondary plant

systems. The inspectors also verified that: (1) any design bases, licensing bases, and

performance capabilities of the component would not be degraded as a result of the

modification; (2) the modification did not place the reactor plant in any unsafe

conditions; and, (3) adequate testing was performed to verify the modification functioned

as expected.

b. Findings

Introduction. A Green self revealing NCV of Technical Specification 6.8.1.a was

identified for the failure to correctly implement a modification to the reactor coolant

sample sink.

Description. On August 23, 1995, the licensee initiated a design change to provide

online sampling capabilities for reactor coolant system hydrogen, oxygen, pH, and

conductivity for Unit 2. The intent of the modification was to divert a portion of reactor

coolant flow to hydrogen, oxygen, pH, and conductivity analyzers and then direct the

effluent to the low level radioactive waste drain header. While walking down the system

to prepare a field sketch of the modification, the responsible engineer incorrectly

identified the header to the main feedwater pump seal drain tank as the low level

radioactive waste drain header. The inspectors reviewed the modification package and

determined that the text description had correctly specified that the effluent would

discharge to the radioactive waste system.

The modification was issued on April 2,1997, and was worked in several phases over

the following 6 years with final connections being performed in August 2003. During this

time, three different responsible engineers and six different instrumentation and control

technicians worked various portions of the modification. The error with the field sketch

was not identified during the installation of the modification. From April 3, 2003, through

April 4, 2004, the licensee performed testing of the modification using demineralized

water. Licensee personnel performed their first test of the analyzers using reactor

coolant on April 7, 2004. The test was terminated after approximately 45 minutes due to

improper operation of the oxygen analyzer. Following repairs to the oxygen analyzer,

the test was again performed on April 14, 2004. During each test, approximately

25 liters of reactor coolant was allowed to flow through the sample piping to the main

feedwater pump seal water drain tank and eventually into the main condenser. The

curie content of the reactor coolant passing through the sample line during the first test

was approximately 2.66 x 10-2 curies. The curie content of the reactor coolant during

the second test was 2.76 x 10-2 curies. Approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> following the termination

of each test, the steam generator radiation monitors generated the Unit 2 control room

"Steam Generator B Blowdown Rad Monitor Hi" annunciator alarm. Approximately

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after the second test, the licensee was able to determine reactor coolant had

reached the main feedwater pump seal water drain tank and was circulated throughout

the secondary plant generating the steam generator radiation monitor alarms. The

licensee placed danger tags on the isolation valves associated with this modification to

prevent additional reactor coolant from reaching the secondary plant.

Enclosure

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Analysis. The inspectors determined this finding was greater than minor because it is

analogous to Example 3.a in Appendix E of Manual Chapter 0612 in that the

modification error was significant enough to require rework to resolve design concerns.

Using Appendix D, "Public Radiation Safety Significance Determination Process," of

Manual Chapter 0609, "Significance Determination Process," The inspectors determined

that the finding had very low safety significance (Green) because the licensee was able

to assess the amount and curie content of the reactor coolant introduced into the

secondary plant and there was no dose impact to the public.

Enforcement. Unit 2 Technical Specification 6.8.1.a requires that written procedures be

implemented covering the activities listed in Regulatory Guide 1.33, Revision 2. The

general procedure for the control of maintenance, repair, replacement, and modification

work is Procedure 6000.030. Section 5.0, "Responsibility and Authority," "Control of

Installation," Revision 7, requires inspection of modification work to ensure the

installation process complies with design documents. Contrary to the above, the

licensee did not perform an adequate inspection of the modification work in that: (1) on

February 19, 1997, the responsible engineer for the design modification to the reactor

coolant sample sink incorrectly identified the drain header to be used for the effluent of

the H2/O2 analyzer which led to incorrectly directing the effluent of the H2/O2 analyzer

to the main feedwater pump seal water drain tank, and (2) personnel installing the

modification did not identify that the sample effluent was directed to the main feedwater

pump seal drain tank. Because of the very low safety significance and because the

licensee included this condition in their corrective action program as

CR ANO-2-2004-0772, this violation is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000368/2004003-05, Improperly

Installed Reactor Coolant Sample Sink Modification.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

For the five maintenance activities listed below, the inspectors reviewed the test data

obtained from the field and ensured: (1) the procedures acceptance criteria were

consistent with the Technical Specifications and the supporting license change

application, (2) the results recorded met the test acceptance criteria, and (3) test

deficiencies were recorded and resolved.

  • On June 15, 2004, the inspectors reviewed the postmaintenance testing of the

Unit 2 Containment Spray Pump 2P-35A following breaker replacement. The

postmaintenance test was in accordance with Procedure 2104.005,

"Containment Spray," Revision 41, Supplement 1.

  • On June 16, 2004, the inspectors reviewed the postmaintenance testing of the

Unit 1 Emergency Feedwater Pump P-7A following a minimum flow recirculation

Enclosure

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line flow valve/orifice modification. The test was in accordance with

Procedure 1106.006, "Emergency Feedwater Pump Operation," Revision 64,

Supplement 12.

  • On June 17, 2004, the inspectors reviewed the postmaintenance testing of Unit 1

Emergency Feedwater Pump P-7B following a minimum flow recirculation line

flow valve/orifice modification. The postmaintenance test was in accordance

with Procedure 1106.006, "Emergency Feedwater Pump Operation,"

Revision 64, Supplement 11.

  • On June 22, 2004, the inspectors reviewed the postmaintenance testing of Unit 2

EDG 2K-4B following replacement of degraded hoses on the gage panel. The

postmaintenance test was in accordance with Procedure 2104.036, "Emergency

Diesel Generator Operations," Revision 47, Supplement 2A.

  • On June 23, 2004, the inspectors reviewed the postmaintenance testing of the

Unit 1 pressurizer emergency relief valve following troubleshooting of an

electrical ground. The postmaintenance test contained in Work

Order 00043411-02 was in accordance with Procedure 1103.005, "Pressurizer

Operation," Revision 30, Supplement 1.

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

Refueling Outage 1R18. The inspectors reviewed the outage safety plan and

contingency plans for the Unit 1 Refueling Outage 1R18, conducted April 20 through

May 13, 2004, to confirm that the licensee had appropriately considered risk, industry

experience, and previous site-specific problems in developing and implementing a plan

that assured maintenance of defense-in-depth. During the refueling outage, the

inspectors observed portions of the shutdown and cooldown processes and monitored

licensee controls over the outage activities listed below:

  • Licensee configuration management, including maintenance of defense-in-depth

commensurate with the outage safety plan for key safety functions and

compliance with the applicable Technical Specifications when taking equipment

out of service

  • Implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing

Enclosure

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  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and an accounting for instrument error

  • Controls over the status and configuration of electrical systems to ensure that

Technical Specifications and outage safety plan requirements were met, and

controls over switchyard activities

and availability of backup processes

  • Controls to ensure that outage work was not impacting the ability of the

operators to operate the spent fuel pool cooling system

alternative means for inventory addition, and controls to prevent inventory loss

  • Controls over activities that could affect reactivity
  • Refueling activities including fuel handling
  • Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the reactor building to verify that debris had not been left which

could block emergency core cooling system (ECCS) suction strainers

  • Licensee identification and resolution of problems related to refueling outage

activities

Unit 1 Main Turbine Forced Outage. On June 11, 2004, in response to elevated noise

levels and vibrations on the main turbine casing, the licensee shut down Unit 1 to

remove and inspect the turbine casing to identify and eliminate the source of the casing

vibrations. The inspectors reviewed the outage plan and contingency plans to confirm

that the licensee had appropriately considered risk, industry experience, and previous

site-specific problems in developing and implementing a plan that assured maintenance

of defense-in-depth. During the outage, the inspectors reviewed computer trends for

portions of the shutdown and cooldown, monitored licensee configuration management,

reviewed controls over the status and configuration of mitigating systems, monitored

controls over activities that could affect reactivity, and reviewed trends associated with

startup and ascension to full power operation. Finally, the inspectors reviewed the

licensee's identification and resolution of problems related to outage activities.

b. Findings

Introduction. The inspectors identified a Green NCV of Unit 1 Technical

Specification 5.4.1.a for the failure to follow procedures for equipment control.

Description. On April 20, 2004, the inspectors toured portions of Unit 1 to determine if

outage preparations for Refueling Outage 1R18, commencing later that day, had any

Enclosure

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adverse affect on plant operation. The inspectors identified that danger tags were hung

on components associated with a number of ECCS systems and trains. Specifically, the

inspectors observed that danger tags were hung on MOVs associated with both trains of

emergency feedwater, high pressure injection, reactor building spray, and other

components. The hanging of these tags was conducted on April 19 and 20, 2004.

The inspectors questioned operations and work control personnel about the condition of

the equipment. The station personnel stated that equipment had been "tagged out"

prior to the outage in an effort to expedite work release. Components which would not

be operated, and were presently in the condition needed for the outage work control

process, were danger tagged in advance of the outage. The personnel stated that the

MOVs were an official tagging boundary and were part of the overall system or

component tagout that would be activated later. This process also included the

MOV handwheels for suction valves, discharge valves, and associated support systems

(such as service water flow) for the ECCS trains. The MOV handwheel danger tags

stated no required position of the valve itself but had the instruction "Do Not Operate."

The inspectors were told this process permitted the equipment to be tagged in advance,

and would not really affect ECCS operation because the equipment would respond to

actuation signals, and could be manually operated under administrative controls

(i.e., upon removing tags). Upon further discussion with operations personnel and

management, the inspectors were informed that the MOV tags did not establish any

boundary and were not to be used as a restriction to remote operation.

The inspectors noted several CRs, including CR ANO-1-2004-1475, where station

personnel questioned this tagging process and demonstrated a lack of understanding of

the new process. The inspectors interviewed operations and maintenance personnel

regarding their understanding of adherence to the tags. The inspectors were informed

that if a change of a tagged MOVs position was required, then removal or temporary lift

of the danger tag must be performed. The inspectors verified that this statement came

directly from Procedure OP-102, "Protective Tagging," Revision 1, Attachment 9.2,

Section 3.7.2. The General Employee Training that was provided to all employees

appeared confusing in that it stated, "You may see an MOV with a tag on its handwheel

stroke open or closed. This is OK since it is not on a tagout with work being performed

until the Real tagout is issued." The inspectors noted a wide range of responses to new

requirements, from an understanding that the tags meant nothing, to the impression that

the equipment could not be operated at all, including remotely. The inspectors were

concerned that the new tagging process could lead to personnel errors.

The inspectors were also concerned about the administrative condition of essential

ECCS equipment isolation valves. While the licensee presented information and

documentation that equipment would still function automatically, and thereby fulfill the

safety function, the inspectors were given only judgmental information regarding the

timeliness of equipment operation under abnormal or accident conditions. The

inspectors determined that administrative removal of the tags could lead to delays in

required local manual operations.

Enclosure

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The inspectors determined that the licensee failed to follow Procedure OP-102,

"Protective Tagging," Revision 1, requirements involving: (1) the use of a partial tagout,

(2) not establishing safety boundaries during the preparation, approval, and hanging of

the tagout, and (3) not providing adequate training to station personnel on the changes

to the tagging process.

Analysis. The inspectors determined that the tagging program failures affected the

mitigating systems cornerstone attribute of equipment availability, and if left uncorrected

the issue could become a more significant safety concern in that a delay in local manual

operation of valves could occur. Using the Phase 1 worksheets in Manual

Chapter 0609, "Significance Determination Process," the finding was determined to

have very low safety significance (Green) because the tagging process did not affect

any automatic safety functions.

Enforcement. Unit 1 Technical Specification 5.4.1.a states that procedures will be

properly implemented for those activities listed in Appendix A of Regulatory Guide 1.33,

Revision 2. In their implementation of "Do Not Operate" tags on Unit 1 during

April 19-20, 2004, the licensee failed to follow numerous aspects of their tagging

Procedure OP-102, "Protective Tagging." Specifically:

  • No section or area of the procedure provided for "partial" tagouts (i.e., the

hanging of some tags now and others at a later date) for an established work

boundary. However, the licensee hung the MOV tags which were part of an

overall outage tagout to be implemented later.

  • Section 5.3 (Tagout Preparation) requires the determination of safety boundaries

for the tagout. As explained to the inspectors, no actual boundaries were

implemented for this tagout. This section also required the hang and restoration

positions of equipment. The "Do Not Operate" tags did not specify a position

and, therefore, did not meet this condition.

  • Section 5.5 (Tagout Approval) requires review to ensure equipment status and

boundary establishment. Again, no boundaries were actually established.

  • Section 5.6 (Hanging Tagouts) requires that first and second persons

independently verify required positions. These tags did not specify a position, so

no verification was performed.

  • Section 5.22 (Training) requires employees be appropriately informed about

changes and revision to the protective tagging procedure. The inspectors

interviews established that training was confusing and inadequate.

Because the failures to correctly implement the tagging program were determined to be

of very low safety significance and has been entered into the licensee's corrective action

program as CR ANO-C-2004-00723, this violation is being treated as an NCV,

Enclosure

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consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000313/2004003-06, Failure to Follow Tagout Procedure in the Use of "Do Not

Operate Tags."

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors assessed the performance of the four surveillance tests listed below.

The inspectors verified that the surveillance tests were performed in accordance with

approved licensee procedures and met Technical Specifications requirements. In

addition, the applicable test data was also reviewed to verify that Technical

Specifications, Updated Final Safety Analysis Report, and licensee procedure

requirements were met.

  • On March 31, 2004, the inspectors reviewed the documentation for the quarterly

surveillance of High Pressure Injection Pump P-36C which was performed on

March 30, 2004. This test was performed in accordance with

Procedure OP-1104.002, Revision 57, Supplement 5, and Work Order

Package 50689580.

  • On March 31, 2004, the inspectors reviewed the monthly surveillance of Unit 2

EDG 2K-4B. This test was performed in accordance with

Procedure OP-2104.036, Revision 47, Supplement 2A.

  • On April 5, 2004, the inspectors reviewed the documentation for the quarterly

surveillance of Service Water Pump 2P-4B which was performed on

March 26, 2004. This test was performed in accordance with

Procedure OP-2104.029, Revision 53, Supplement 1B.

  • On June 3, 2004, the inspectors reviewed the documentation for the 18-month

surveillance of the pressurizer electromatic Relief Valve PSV-1000. This test

was performed in accordance with Procedure OP-1103.005, Revision 30,

Supplement 1.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the two temporary alterations listed below to assess the

following attributes: (1) the adequacy of the safety evaluation; (2) the consistency of the

installation with the modification documentation; (3) the updating of drawings and

procedures, as applicable; and (4) the adequacy of post-installation testing. Also, the

Enclosure

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inspectors confirmed that these temporary modifications were implemented and

installed as authorized by Procedure 1000.028, "Control of Temporary Alterations,"

Revision 23.

  • Temporary alteration to remove Door 48, red train south vital switchgear room to

turbine building door per Work Order 50244579 to support maintenance for

pulling electrical cabling for Service Water Pump 2P-4B in Unit 1. The door

removal was evaluated under Engineering Request ER-ANO-2004-0014-000.

  • Temporary alteration to install auxiliary heating for ensuring safety-related

battery operability in the EDG corridor in Unit 2. The heater installation was

evaluated under Engineering Request ER-ANO-2002-0145-000.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness (EP)

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspector performed an in-office review of Revision 29 to the ANO Emergency Plan

submitted November 2003. The revision included removal of the Arkansas Department

of Health as a notification recipient in favor of direct notification to local officials,

clarification of off-site responsibilities, incorporation of previous changes to the

emergency action levels, removal of specific reference to the type of radios used for

public alerting, update of the evacuation time study and letters of agreement, removal of

specific methods of performing functions such as providing public information and

distribution of tone alert radios, and other administrative and editorial changes.

The revision was compared to the previous revisions, to the criteria of NUREG-0654,

"Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants," Revision 1, and to the requirements

of 10 CFR 50.47(b) and 50.54(q) to determine if the revisions decreased the

effectiveness of the plan. The inspector completed one sample during the inspection.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

Enclosure

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2OS1 Access Control To Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspector used the

requirements in 10 CFR Part 20, the Technical Specifications, and the licensees

procedures required by Technical Specifications as criteria for determining compliance.

During the inspection, the inspector interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspector performed

independent radiation dose rate measurements and reviewed the following items:

  • Controls (surveys, posting, and barricades) of three radiation, high radiation, or

airborne radioactivity areas

  • Radiation work permit, procedure, and engineering controls and air sampler

locations

  • Conformity of electronic personal dosimeter alarm set points with survey

indications and plant policy; and workers knowledge of required actions when

their electronic personnel dosimeter noticeably malfunctions or alarms.

  • Physical and programmatic controls for highly activated or contaminated

materials (nonfuel) stored within spent fuel and other storage pools.

  • Self-assessments and audits related to the access control program since the last

inspection

  • Corrective action documents related to access controls
  • Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls such as required surveys, radiation protection

job coverage, and contamination controls during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

Enclosure

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The inspector reviewed the following areas; however, because the conditions did not

exist or an event had not occurred, there were no specific examples to review:

  • Performance indicator (PI) events and associated documentation packages

reported by the licensee in the occupational radiation safety cornerstone

areas

  • Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

  • Licensee event reports (LERs) and special reports related to the access control

program since the last inspection

  • Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

and very high radiation areas

The inspector completed 21 of the required 21 samples.

b. Findings

Introduction. The inspector identified a Green self revealing NCV of Unit 2 Technical

Specification 6.13.1 involving the licensees failure to post and control high radiation

areas.

Description. After workers reported "abnormal" electronic dosimeter readings on

October 14, 2003, the licensee identified an uncontrolled high radiation area in the Unit 2

sample cooler room. The licensees subsequent review determined: (1) on

October 12, 2003, chemistry personnel notified radiation protection personnel of

increased reactor coolant system radioactivity, (2) also on October 12, 2003, radiation

protection personnel posted the rooms beside and below the Unit 2 sample cooler room

(the primary sample room and the Charging Pump Room 2P-36) as high radiation areas,

and (3) the lack of written documentation was the likely cause for this condition not being

identified prior to the workers entering the area. Based on this information, the inspector

concluded that the licensee had sufficient information and should have identified and

controlled the high radiation area on October 12, 2003. The finding is considered to be

self-revealing because the licensee was alerted to the situation by circumstances outside

its normal process for identifying high radiation areas.

Analysis. The failure to control a high radiation area is a performance deficiency. This

finding was greater than minor because it was associated with one of the cornerstone

attributes and affected the cornerstone objective, in that, inadequate controls of high

Enclosure

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radiation areas affected the licensees ability to ensure adequate protection of worker

health and safety from exposure to radiation. Because the finding involved the potential

for workers to receive significant, unplanned, unintended dose as a result of conditions

contrary to Technical Specification requirements, the inspector used the occupational

radiation safety significance determination process described in Manual Chapter 0609,

Appendix C, "Occupational Radiation Safety Significance Determination Process," to

analyze the significance of the examples. The inspector determined that the finding was

of very low significance because it did not involve (1) ALARA planning and controls,

(2) an overexposure, (3) a substantial potential for overexposure, or (4) an impaired

ability to assess dose. The issue involved human performance cross-cutting aspects

associated with the thoroughness of radiation surveys by radiation protection personnel.

Enforcement. Unit 2 Technical Specification 6.13.1 states, "Pursuant to 20.1601(c), in

lieu of the requirements of 20.1601(a), each high radiation area, as defined in

10 CFR Part 20, in which the intensity of radiation is greater than 100 millirem per hour,

but equal to or less than 1000 millirem per hour at 30 centimeters from the radiation

source or from any surface which the radiation penetrates shall be barricaded and

conspicuously posted as a high radiation area and the entrance thereto shall be

controlled by radiation work permit." Contrary to this, the licensee did not barricade,

post, and control a high radiation area in the Unit 2 sample cooler room. Because the

failure to correctly control high radiation areas was determined to be of very low safety

significance and has been entered into the licensees corrective action program as

CR 2-2003-01643, this violation is being treated as an NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy: NCV 05000368/2004003-07, Failure to

Control a High Radiation Area.

4. OTHER ACTIVITIES

4OA1 PI Verification (71151)

a. Inspection Scope

The inspectors sampled licensee submittals for the four PIs listed below for the period

from April 1, 2003 through March 30, 2004. The inspectors verified: (1) the accuracy of

the PI data reported during that period and (2) used the PI definitions and guidance

contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 2, to

verify the basis in reporting for each data element.

Reactor Safety Cornerstone

The inspectors reviewed operator log entries, daily shift manager reports, plant computer

data, CRs, maintenance action item paperwork, maintenance rule data, and PI data

sheets to determine whether the licensee adequately verified the PIs listed above. This

number was compared to the number reported for the PI during the past 3 quarters.

Enclosure

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Also, the inspectors interviewed licensee personnel responsible for compiling the

information.

Occupational Radiation Safety Cornerstone

  • Occupational Exposure Control Effectiveness PI

Licensee records reviewed included corrective action documentation that identified

occurrences of locked high radiation areas (as defined in Technical Specification 6.13.2),

very high radiation areas (as defined in 10 CFR 20.1003), and unplanned personnel

exposures (as defined in NEI 99-02). Additional items reviewed included radiological

control area entry and electronic dosimeter alarm setpoints. The inspector interviewed

licensee personnel that were accountable for collecting and evaluating the PI data. In

addition, the inspector toured plant areas to verify that high radiation, locked high

radiation, and very high radiation areas were properly controlled.

Public Radiation Safety Cornerstone

  • Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

Licensee records reviewed included corrective action documentation that identified

occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and

those reported to the NRC. The inspector interviewed licensee personnel that were

accountable for collecting and evaluating the PI data.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

1. Annual Sample Review

a. Inspection Scope

The inspectors chose one issue for more in depth review to verify that licensee personnel

had taken corrective actions commensurate with the significance of the issue. The issue

and its bases for selection is described below:

  • In 2002 during Refueling Outage 2R15, ANO management assigned Unit 2

personnel to work overtime in excess of Technical Specification limits under

blanket authorizations. This practice led to a NCV in NRC Inspection

Report 05000313/2002002; 05000368/2002002. The inspectors reviewed

CR ANO-2-2002-1339 which the licensee used to correct the issue and

questioned its effectiveness. The inspectors reviewed protected area ingress and

Enclosure

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egress records, interviewed numerous licensee personnel, and reviewed overtime

authorization forms from Refueling Outage 1R18 to determine if the corrective

action program adequately resolved the issue.

When evaluating the effectiveness of the licensees corrective actions for this issue, the

following attributes were considered:

  • Complete and accurate identification of the problem in a timely manner

commensurate with its significance and ease of discovery

  • Evaluation and disposition of operability and reportability issues
  • Consideration of extent of condition, generic implications, common cause, and

previous occurrences

  • Classification and prioritization of the resolution of the problem commensurate

with its safety significance

  • Identification of root and contributing causes of the problem for significant

conditions adverse to quality

  • Identification of corrective actions which are appropriately focused to correct the

problem

  • Completion of corrective actions in a timely manner commensurate with the safety

significance of the issue

b. Findings and Observations

No findings of significance were identified. While the inspectors found that the licensee

had corrected the widespread assignment of overtime, they did find two isolated

instances where the licensee's program for the control of overtime was not thorough.

These instances involved isolated examples of: (1) working in excess of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in a

48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> period without prior authorization, and (2) not meeting the definition of very

unusual circumstances for authorized overtime as set forth in Generic Letter 82-12.

2. Cross-References to Problem Identification and Resolution (PI&R) Findings Documented

Elsewhere

Section 1R04 documents a condition where the licensee did not take corrective actions to

assure that uncalibrated valve position indicators for HPSI and LPSI MOVs were not

being used in procedures to operate Unit 2.

Section 1R15 documents a condition where the licensee was not taking timely corrective

actions to clean discolored boric acid off of a Unit 2 containment spray pump.

Section 4OA3 documents a condition where licensee personnel did not implement

Enclosure

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effective corrective actions to address abnormal conditions in the main turbine lube oil

system in Unit 1. As a result, an operator tripped the reactor as a result of confusing

indications brought about by the failure to correct the abnormal condition.

3. Semi-Annual Trend Review

a. Inspection Scope

On June 23, 2004, the inspectors completed a semi-annual review of licensee internal

documents, reports, audits, and PIs to identify trends that might indicate the existence of

more significant safety issues. The inspectors reviewed the following:

  • system health indicators

C temporary alterations

C CRs

  • work requests
  • maintenance rule failures

b. Findings

No findings of significance were identified. However, during the review, the inspectors

observed the following issues which were discussed with licensee management:

C Licensee personnel documented 17 instances where personnel discovered

amounts of transient combustibles to be in excess of the prescribed

administrative limits set for the associated area. Four of these administrative limit

violations were identified by NRC inspectors. The inspectors considered these

issues minor since the fire hazards analysis limits were not violated, but also

considered the large number of instances to be indicative of the existence of a

programmatic problem in the control of combustible materials which could result

in large amounts of uncontrolled combustibles. The inspectors considered this

trend to be examples of poor human performance by multiple disciplines in that

the combustibles limits were exceeded by different departments. Licensee

management was aware of this performance issue and has implemented

corrective actions as set forth in CR ANO-C-2004-0909.

C Licensee personnel documented several dozen instances where training has

either lapsed, been inadequate, missed, not performed, incorrectly processed,

inappropriately tracked, or incorrectly documented. The number of instances and

the variety of the issues have the potential for: (1) using unqualified or

undertrained individuals to perform work, (2) reducing the quality of workmanship,

and (3) and challenging Technical Specifications manning requirements. None of

these instances have actually challenged plant reliability, but the number of

findings is indicative of a need for improved oversight of training. Licensee

management was aware of this performance issue and has implemented

corrective actions as set forth in CR ANO-C-2003-0647 and

CR ANO-C-2004-0063.

Enclosure

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C Licensee personnel documented numerous instances where too much lube oil

was added to equipment important to safety. For example, Emergency Control

Room Chillers 2VE-1A and 2VE-1B, Diesel Fire Water Pump P-6B, Unit 2

EDGs 2K-4A and 2K-4B, and the Unit 2 Emergency Feedwater Turbine 2K-3

were all found to have excess oil added and required an evaluation for operabilty.

None of the components were determined to be inoperable, but the inspectors

considered the numerous amount of instances to have the potential for making a

component inoperable due to an excessive addition of oil in the future. Licensee

management was aware of this performance issue and have implemented

corrective actions as set forth in CR ANO-C-2004-0526.

4. PI&R Review of Access Control to Radiologically Significant Areas

During the performance of Inspection Procedure 71121.01, the inspector evaluated the

effectiveness of the licensees PI&R processes regarding access controls to

radiologically significant areas and radiation worker practices. While comparing the root

cause analysis and the corrective action assignments associated with CR 2-2003-01405,

the inspector noted that all planned corrective actions were not implemented.

Specifically, an action to address one contributing cause stated, "Incorporate lessons

learned training of this event into Operations Continuing Training Program. . . ." The

action was approved by the corrective action review group and assigned a due date of

March 11, 2004; however, a subsequent action assignment was not added to the CR.

Licensee representatives confirmed that the corrective action was not implemented. In

response, the licensee initiated CR 2-2004-00872 to document the problem.

4OA3 Event Followup (71153)

1. (Closed) LER 05000313/2002001-00, Main Steam Safety Valve As-Found Lift Settings

were not Within Technical Specifications Limits

On September 27, 2002, prior to the upcoming scheduled Refueling Outage 1R17,

planned surveillance testing revealed the as-found setpoints for three of the eight main

steam safety valves on the Steam Header A and five of the eight main steam safety

valves on the Steam Header B were outside the limits provided by the Unit 1 Technical

Specifications. Three of the main steam safety valves actual lift settings were in excess

of the +3 percent nominal setpoint limit. The remaining five main steam safety valves

actual lift settings were below the -3 percent nominal setpoint limit. The licensee initiated

CRs ANO-1-2002-1088 and -1089, conducted a root cause investigation, and performed

subsequent testing of installed and spare safety valves. The licensee determined that

the combination of spindle run-out and the change in test method was the root cause.

These CRs and their associated root cause investigation were reviewed by the

inspectors. This finding constituted a violation of minor significance because the

as-found setpoints were bounded by the accident analysis assumptions. This LER is

closed.

Enclosure

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2. (Closed) LER 05000313/2002002-00: Main Turbine Trip due to Binding of the

Mechanical Trip Spool Valve Resulted in an Automatic Actuation of the Reactor

Protection System

a. Inspection Scope

The inspectors reviewed the LER and corrective action document CR ANO-2-2002-1144

which documented this event and the circumstances which led to it, to verify that the

cause of the October 4, 2002, Unit 1 reactor trip event was identified and that corrective

actions were reasonable. The reactor trip was caused by an operator who released the

main turbine test lever with a turbine trip signal still in effect. The inspectors reviewed

plant parameters and verified that licensee staff properly implemented the appropriate

plant procedures and that plant equipment performed as required. The inspectors also

reviewed the cause of the sequence of events dating back to the original indication of

equipment problems.

b. Findings

Introduction. A self revealing Green finding was identified for the failure of personnel to

correct the cause of contaminants in the Unit 1 main turbine lube oil system.

Description. The inspectors discovered that prior to October 2002, the licensee had

found and documented the following problems with the operation of the Unit 1 main

turbine front standard levers:

  • In March 1993, while performing maintenance, the low bearing oil trip failed to trip

the main turbine on Unit 1. CR ANO-1-1993-0083 was initiated and its corrective

actions included testing the trip block during the shutdown and subsequent

startup and increasing the frequency of testing of the trip block to semi-annually.

  • In May 1996, the latch/trip lever for the main turbine did not trip.

CR ANO-1-1996-0185 was initiated and its corrective actions included increasing

testing frequency of the trip block to quarterly.

  • In March 2002, the trip pressure for low condenser vacuum and low bearing oil

pressure were outside the acceptable ranges. The cause was attributed to a

sticking latch/trip lever or sticking of its associated spool. CR ANO-1-2002-0398

was initiated which included corrective actions of scheduling another trip test

before summer 2002 and exercising the latch/trip lever.

All of these instances with trouble in the main turbine lube oil system were addressed by

increasing the test frequency of the front standard or exercising the affected

components. No corrective actions were aimed at determining what was causing the

sticking components and preventing recurrence.

On October 4, 2002, with Unit 1 at 42 percent power and in the process of shutting down

for Refueling Outage 1R17, the licensee was performing Procedure 1106.009, "Turbine

Enclosure

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Oil Trip Test," Supplement 4, "Turbine Startup (Warmup and Roll)," Revision 31, to test

the main turbine lube oil system. During the low vacuum and low bearing oil trip portion

of the test, the latch/trip lever did not move when the trips occurred. Despite this

abnormality, licensee personnel continued with the overspeed trip test.

The test lever was then taken to the test position to override the overspeed trip to inhibit

a turbine trip during the test. When the overspeed trip test condition was initiated, the

latch/trip lever moved slightly towards the trip position. One of the two local operators

attempted to reset the trip by positioning the latch/trip lever to the reset position, but felt

resistance in the movement of the lever. After discussions with instrumentation and

controls personnel, the operator again attempted to reset the latch/trip lever, but again

encountered resistance in movement of the lever. The resistance in the trip lever was an

indication that water contamination was interfering with the lever operation. The

operator again had discussions with instrumentation and controls personnel. The second

operator then ordered the release the of the test lever. Because the trip lever was

sticking, the turbine trip had not been reset. Consequently when the test lever was

released the turbine trip occurred, and as a result, the reactor tripped.

Analysis. The finding is greater than minor because it was analogous to Example 4.d in

Appendix E, "Examples of Minor Issues," of Manual Chapter 0612, "Significance

Determination Process," in that the failure to take adequate corrective action contributed

to an operator error. Using the Phase 1 worksheet in Manual Chapter 0609,

"Significance Determination Process," the finding was determined to have very low safety

significance (Green) because, although it resulted in a reactor trip, no other complicating

events were caused by the error and all mitigating systems remained available to the

operators.

Several human performance cross-cutting errors were made which contributed to this

finding. First, the operator who was conducting the test later stated that he was only

90 percent certain that the turbine trip had reset, but decided to proceed. Second,

despite previous questionable results earlier in the test when the latch/trip lever did not

move, the operator decided to continue with the test. Third, the operator never raised

either of the first two issues to the on-duty control room supervisor or shift manager.

Inclusion of these personnel could have allowed a power reduction of approximately

1 percent to avert a reactor trip or even allow the control room staff to be prepared for the

reactor trip.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because it occurred on

non-safety secondary plant equipment. Licensee personnel entered this issue into the

corrective action program as CR ANO-1-2002-1144. FIN 05000313/2004003-08, Failure

to Implement Corrective Actions for Turbine Lube Oil System.

Enclosure

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4OA4 Cross Cutting Aspects of Findings

Cross-Reference to Human Performance Findings Documented Elsewhere

Section 1R04 describes a condition where HPSI and LPSI valve indicators in Unit 2 were

left uncalibrated for approximately 8 years yet were still referenced for use in plant

procedures.

Section 1R05 describes a finding where operations personnel staged inadequate

equipment as a compensatory action for degraded firefighting equipment upon loss of all

manual and automatic suppression to the intake structures.

Section 4OA2 documents a trend where numerous groups across the site have

repeatedly violated the administrative limits for loading of transient combustibles in

various areas throughout both units. Also documented were the repeat instances of

overfilling components with oil and inadequate training.

Section 4OA3 describes a finding in which a reactor trip was caused by ineffective

corrective actions for problems with the main turbine trip oil system. The inspectors

noted several human performance errors which led to a turbine trip and reactor trip.

Section 4OA5 describes a finding where human errors in the performance of the

inspection of the lower reactor vessel head penetration nozzles led to an incomplete

inspection.

4OA5 Other Activities

1. (Closed) Unresolved Item (URI)05000368/2003005-04, Design Deficiencies with

Mechanical Nozzle Seal Assemblies (MNSAs)

During the Unit 2 Refueling Outage 2R16 in September 2003, licensee personnel

discovered leakage from one of the MNSAs that was installed on certain pressurizer

heater sleeves to prevent the recurrence of leakage. As part of the inspection effort for

this occurrence, regional NRC personnel conducted a review of the design of the MNSA

and its installation on the Unit 2 pressurizer. The inspectors found nonconservatisms in

the analyses for the MNSA, but the licensee demonstrated and the NRC confirmed that

adequate safety margin remained in the design such that ASME Code requirements

were met. The licensee documented the problems in CR ANO-2-2003-0070. This URI is

closed.

2. Temporary Instruction (TI) 2515/145/150, "Reactor Pressure Vessel Head and Vessel

Head Penetration Nozzles"

In October 2002, the inspectors completed the review of the licensees Unit 1 reactor

pressure vessel head bare metal visual examination using TI 2515/145. This review was

documented in NRC Inspection Report 0500313/2002-05. TI 2515/145 was not

performed on Unit 2. Per TI 2515/150, Section 07, "Expiration," the October 2002

Enclosure

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completion of TI 2515/145 was credited as one of the two required TI 2515/150 reviews.

Therefore, TI 2515/145 is closed for Units 1 and 2.

3. Temporary Instruction (TI) 2515/152, "Reactor Pressure Vessel Lower Head Penetration

Nozzles"

a. Inspection Scope

On April 23, 2004, the inspectors completed the review of the licensees Unit 1 reactor

pressure vessel lower head bare metal visual examination. The inspectors reviewed the

licensee's videotape for evidence of boric acid deposits on the lower reactor vessel head.

Unit 2 has no bottom mounted penetration nozzles and thus is exempt from inspection

under Temporary Instruction 2515/152. The completion of the Unit 1 Reactor Pressure

Vessel Lower Head Penetration inspection closes out TI 2515/152 for Arkansas Nuclear

One.

b. Findings

Introduction: The inspectors identified a Green NCV of Unit 1 Technical

Specification 5.4.1.a for the failure to perform a complete examination of the lower

reactor vessel head.

Description: The inspection of the lower reactor vessel head was performed using a

video camera mounted on a very small robotic crawler (about 2-3" long) which was

magnetically attached to the lower vessel head and looked up at the nozzles and down at

the insulation below. A certified Level III nondestructive examiner performed the

examination. The examination was conducted in accordance with Procedure 2311.09,

"Unit 1 and Unit 2 Alloy 600 Inspection," Revision 5.

The inspectors determined that: (1) the inspection provided 360 degree coverage of all

the nozzles, (2) the licensee could identify small boric acid leaks as described in

Bulletin 2003-02, "Leakage from Reactor Pressure Vessel Lower Head Penetrations and

Reactor Coolant Pressure Boundary Integrity," (3) licensee personnel were able to

disposition and resolve identified deficiencies, (4) licensee personnel could determine if

there was any pressure boundary leakage or reactor pressure vessel lower head

corrosion as described in the bulletin, (5) the clarity of the video was good and the

lighting was adequate, and (6) insulation and instrumentation were not impediments.

The inspectors noted that the head did have boric acid stains which the licensee

attributed to cavity seal ring leakage during past refueling outages. The licensee did not

take any chemical samples of the deposits. There were several locations with flaking

high temperature paint and associated corrosion as a result of the past refueling outage

cavity seal ring leakage. The licensee appropriately dispositioned the traces of boric acid

and flaking paint in their corrective action program. The licensee's examiners were able

to verify that there were no leaks in the annulus regions between the bottom head and

penetration piping. No material deficiencies that required repair were noted during the

inspection of the lower reactor vessel head.

Enclosure

-31-

The inspectors identified two impediments for completing a successful inspection of the

lower head. First, no landmark or reference point was used to identify each specific

nozzle while the inspection progressed. Second, the crawler had an upward view of the

inspection surface while the nozzle location map viewpoint was from above.

During the review of the videotape, the inspectors determined that the licensees

examiner lost place-keeping after inspecting 18 of the 52 lower head nozzles. As a

result, at least one nozzle was not fully inspected and approximately 24 nozzles were

misidentified on the videotape. A significant cause of this loss of placekeeping was the

lack of references for the crawler mounted video camera operator.

As a result of concerns raised by the inspectors with performing the bare metal

inspection of the bottom mounted instruments, the licensee performed a more in-depth

verification of the inspection of the already completed reactor upper head control rod

drive mechanisms (CRDM) nozzles. The licensee's review discovered that a

100 percent inspection of the upper head nozzles was not obtained on the initial

performance of Procedure 2311.009. This inspection demonstrated that the crawler

mounted video camera operator became misoriented and thus all or portions of

15 CRDMs did not receive a full 360o inspection. The licensee's investigation for these

missed inspection items identified several causes that involved, in part: (1) a lack of

adequate verification and review practices, (2) an inadequate inspection plan,

(3) inconsistent crawler paths, and (4) inadequate direction to ensure the video was

correctly captured if unexpectantly interrupted.

Analysis. The inspectors determined that this finding was greater than minor since it

affected the barrier integrity cornerstone objective for providing reasonable assurance

that physical design barriers protect the public from radionuclide releases caused by

accidents or events. Using the Phase 1 worksheets in Manual Chapter 0609,

"Significance Determination Process," the issue was determined to have very low safety

significance (Green) because no actual leakage from the reactor vessel penetrations was

identified on subsequent inspections. This issue involved human performance

cross-cutting aspects associated with inattention to detail by engineering personnel

during inservice examinations.

Enforcement. Unit 1 Technical Specification 5.4.1.a requires that the licensee establish

and implement written procedures recommended in Regulatory Guide 1.33, Revision 2,

Appendix A, February 1978 which required procedures for inspections of the reactor

coolant system pressure boundary. Attachment 1 of ANO Procedure 2311.009,

Step 8.1.7, required that the licensee inspect each incore instrument nozzle at the

reactor vessel bottom penetrations for indication of RCS leakage. Contrary to this, the

licensee did not inspect 100 percent of the lower head nozzles during their initial

inspection of the lower reactor vessel head nozzle penetrations in Refueling

Outage 1R18. This finding was of very low safety significance and has been entered into

the licensees corrective action program as CR 1-ANO-2004-0827; therefore, it is being

Enclosure

-32-

treated as a NCV consistent with Section VI.A of the NRC Enforcement Policy

(NCV 05000313/2004003-09), Failure to Follow Reactor Vessel Bottom Head Inspection

Procedure.

4. TI 2515/153, "Reactor Containment Sump Blockage (NRC Bulletin 2003-01)"

a. Inspection Scope

On June 18, 2004, the inspectors completed a review of the licensees implementation of

compensatory measures for the Unit 1 and 2 containment recirculation sumps. The

compensatory measures were delineated in Entergy's response to NRC Bulletin 2003-01,

Letter 0CAN080302, "60-Day Response to NRC Bulletin 2003-01, Potential Impact of

Debris Blockage on Emergency Sump Recirculation at Pressurized Water Reactors,"

dated August 7, 2003, and Letter 0CAN060402, "NRC Bulletin 2003-01 Additional

Information," dated June 10, 2004. In these letters, Entergy described measures that

have been implemented to reduce the potential risk of ECCS and containment spray

system degradation. These measures addressed:

  • Providing operator training on indications of and responses to sump clogging
  • Implementing procedure modifications that would delay switchover to the

containment sump recirculation

  • Ensuring alternate water sources are available to refill the refueling water storage

tank

  • Implementing more aggressive containment cleaning and increased foreign

material controls

  • Ensuring containment drainage paths are unblocked
  • Ensuring sump screens are free of adverse gaps and breaches

In addition to reviewing the licensees response to NRC Bulletin 2003-01, the inspectors

reviewed the licensees programs and procedures for performing containment walkdowns

and controlling containment coating and insulating materials. Additionally, the inspectors

performed containment walkdowns during outages on Unit 2 on February 7, 2004, and

Unit 1 on May 8, 2004, to quantify potential debris sources and to check for gaps in the

sumps screened flowpath. The inspectors also viewed the internal portions of the Unit 1

containment sump several times during routine containment walkdowns conducted

during Refueling Outage 1R18.

The inspectors observed the installation of one sump-related modification for Unit 1,

which was implemented during Refueling Outage 1R18, to address concerns of spalling

and cracking of the concrete liner. The licensee installed a stainless steel liner to prevent

Enclosure

-33-

any future complications from the degrading concrete. The TI 2515/153, inspections are

complete for Units 1 and Unit 2.

b. Findings

No findings of significance were identified.

5. TI 2515/156, "Offsite Power System Operational Readiness"

a. Inspection Scope

The inspectors collected data from licensee maintenance records, event reports,

corrective action documents and procedures and through interviews of station

engineering, maintenance, and operations staff as required by TI 2515/156. The data

was gathered to assess the operational readiness of the offsite power systems in

accordance with NRC requirements such as Appendix A to 10 CFR Part 50, General

Design Criterion (GDC) 17; Criterion XVI of Appendix B to10 CFR Part 50; Plant

Technical Specifications (TS) for offsite power systems; 10 CFR 50.63;

10 CFR 50.65(a)(4); and licensee procedures. Documents reviewed for this TI are listed

in the attachment under Section 4OA5.

b. Findings

No findings of significance were identified. Based on the inspection, no immediate

operability issues were identified. In accordance with TI 2515/156 reporting

requirements, the inspectors provided the required data in the work sheets provided with

the TI to the headquarters staff for further analysis. This completes the inspection

requirements for TI 2515/156.

4OA6 Meetings, Including Exit

On May 7, 2004, a regional inspector presented the results of the inspection of access

control to radiologically significant areas to Mr. J. Forbes, Vice President, Operations and

other members of his staff. The licensee acknowledged the inspection findings.

On May 7, 2004, a regional inspector presented the results of the inspection of

nondestructive examination and steam generator tube inspection activities to

Mr. J. Forbes, Vice President, Operations, and other members of his staff. The licensee

acknowledged the inspection findings.

On May 27, 2004, regional inspectors presented the results of the permanent plant

modifications inspection to Mr. J. Kowalewski, Director, Engineering, and other licensee

employees. The licensee acknowledged the inspection findings.

On June 3, 2004, a regional inspector conducted an exit interview by telephone, and

presented the inspection results from their review of emergency plan changes to

Mr. R. Holeyfield, Emergency Preparedness Manager. The licensee acknowledged the

Enclosure

-34-

inspection findings.

On June 30, 2004, the resident inspectors presented the results of their inspections to

Mr. C. Eubanks, General Manager, Plant Operations, and other members of the

licensees management staff. The licensee acknowledged the inspection findings.

All of the inspectors noted that while proprietary information may have been reviewed,

none would be included in this report.

40A7 Licensee-identified Violations

The following violation of very low significance (Green) was identified by the licensee and

is a violation of NRC requirements which meet the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting quality

shall be accomplished in accordance with prescribed instructions. From February 2-6

and February 16-20, 2004, during the respective Unit 2 red and green train EDG

extended allowed outages, the licensee did not control transient combustibles in the

diesel corridor, Fire Area 2109-U to the zero level as prescribed in Procedure OPS-146,

"Extended EDG Outage Coordinator Checklist." A heater which was part of a temporary

alteration for battery room temperature control was left in the corridor, thereby,

introducing transient combustibles which were not controlled. This condition is described

in the licensees corrective action program in CR ANO-2-2004-0821. This finding is of

very low safety significance because the amount of added combustibles did not exceed

the amount assumed in the licensees fire hazards analysis.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. Beaird, Supervisor, Systems Engineering

S. Bennett, Licensing Specialist

B. Berryman, Manager, Planning and Scheduling

C. Chadburn, Supervisor, Design Engineering

L. Compton, Manager, Engineering Programs and Components

S. Cotton, Manager, Training

G. Dobbs, Supervisor, Design Engineering

C. Eubanks, General Manager, Plant Operations

J. Forbes, Vice President, Operations

F. Forrest, Unit 1 Operations Manager

R. Gordon, Manager, Systems Engineering

A. Hawkins, Licensing Specialist

A. Heflin, Unit 2 Operations Manager

J. Hoffpauir, Manager, Maintenance

R. Holeyfield, Manager, Emergency Planning

B. James, Manager, Alloy 600 Project

D. James, Manager, Licensing

J. Kowalewski, Director, Engineering

R. Lingle, Plant Manager, Operations

D. Meatheany, Steam Generator Lead, Engineering Projects and Components

J. Miller, Manager, Nuclear Engineering Design

T. Mitchell, Director, Nuclear Safety Assurance

K. Nichols, Manager, Design Engineering

G. Parks, Supervisor, Quality Control/Nondestructive Examination

R. Partridge, Manager, Technical Support

B. Patrick, Manager, Radiation Protection

S. Pyle, Licensing Specialist

R. Schwartz, Specialist, Radiation Protection

R. Scheide, Licensing Specialist

W. Sims, Supervisor, Design Engineering

C. Tyrone, Manager, Quality Assurance

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000368/2004003-01 NCV Failure to correct inaccurate HPSI and LPSI valve position

indications (Section 1R04)05000313/2004003-02 NCV Failure to provide adequate compensatory measures for a

05000368/2004003-02 loss of fire water to the intake structure (Section 1R05)

A-1 Attachment

05000313/2004003-03 NCV Failure to adequately assess risk due to external conditions05000368/2004003-03 (Section 1R13)05000368/2004003-04 NCV Untimely corrective actions to clean discolored boric acid

deposits (Section 1R15)05000368/2004003-05 NCV Improperly installed reactor coolant sample sink modification

(Section 1R17)05000313/2004003-06 NCV Failure to follow tagout procedure in the use of Do Not

Operate tags (Section 1R20)05000368/2004003-07 NCV Failure to control a high radiation area (Section 2OS1)05000313/2004003-08 FIN Failure to implement corrective actions for turbine lube oil

System (Section 4OA3)05000313/2004003-09 NCV Failure to follow reactor vessel bottom head inspection

procedure (Section 4OA5)

Closed

05000368/2003005-04 URI Mechanical nozzle seal assemblies unresolved item

(Section 4OA5)05000313/2002001-00 LER Main steam safety valve as-found lift settings were not within

Technical Specification limits (Section 4OA3)05000313/2002002-00 LER Main turbine Trip due to mechanical trip spool valve resulted

in an automatic actuation of the reactor protection system

(Section 4OA3)

Discussed

None

LIST OF DOCUMENTS REVIEWED

In addition to the documents called out in the inspection report, the following documents were

selected and reviewed by the inspectors to accomplish the objectives and scope of the

inspection and to support any findings:

Section 1R05: Fire Protection (71111.05)

Procedures/Plant Document:

Arkansas Nuclear One Fire Hazards Analysis, Revision 8

A-2 Attachment

Plant Drawings:

FP-101, "Fire Zone Fuel Handling Floor Plan El. 404-0" and 422-6"," Sheet 1, Revision 29

FP-102, "Fire Zone Operating Floor Plan El. 386-0"," Sheet 1, Revision 29

FP-105, "Fire Zone Plan Below Grade El. 335-0"," Sheet 1, Revision 18

Engineering Calculation

85-E-0053-15, Revision 45

Section 1R08: Inservice Inspection (71111.08)

Nondestructive Examinations

Low Pressure Safety Injection Pipe to Ell Circumferential Seam Ultrasonic

Make-up System Recirculation Orifice Radiographic

Reactor Vessel Head Nozzle 61 Liquid Penetrant

Miscellaneous

Arkansas Nuclear One Unit 1 In-Situ Pressure Testing, March 2004

Engineering Report ER-01-R-1001-05, "ANO-1 OTSG 20 Percent Tube Plugging Report,"

Revision 0

Engineering Report ER-ANO-2002-1148-000, "ANO-1 Once Through Steam Generator 1R17

Cycle 18 Operational Assessment," December 2002

Engineering Report ER-ANO-2003-0671-000, "Once-Through Steam Generator Degradation

Assessment for Arkansas Nuclear One Unit 1 1R18," April 2004

Procedure Qualification Record PQR-AS-006, WPS P8-AT-Ag, Revision 9

Procedure Qualification Record PQR-170, "Manual Gas Tungsten & Shielded Metal Arc Welding

(GTAW & SMAW)," Revision 1

Section III, Division 1, Subsection NB, "ASME Boiler and Pressure Vessel Code," 1989 Edition,

No Addenda

Section IX, "ASME Boiler and Pressure Vessel Code," 2001 Edition through 2004 Addenda

TD Y006.0010, "Short Form Catalog for Yokogawa Electrical Indicating Instrumentation,"

Revision 0

Welding Procedure Specification WPS-E-P8-T-A8, Ar, Revision 0

A-3 Attachment

Procedures

54-PT-6-09, "Visible Solvent Removable Liquid Penetrant Examination Procedure," revised

February 11, 2004

5120.500, "Steam Generator Integrity Program Implementation," Change Number 010-00-0

5120.509, "Steam Generator Inservice Inspection Implementation Program," Change 001-03-0

5120.518, "ANO Steam Generator Testing and Repair," Change 001-01-0

5120.519, "ANO Steam Generator In-Situ Testing," Change 001-00-0

NDE9.23, "Ultrasonic Examination of Austenitic Piping Welds (ASME Section XI)," Revision 2

NDE9.55, "Radiographic Examination of ASME, ANSI, AWS, API, AWWA Welds, and

Components," Revision 2

Weld Packages

04-07, "Piping Downstream of Valve SF-56 (Repair)"

04-27, "Valves MU-1025A and MU-1032A/B (Replacement)"

04-73, "Valve SF-32 (Replacement)"

04-98, "Valve RC-1030B (Repair)"

Work Orders

MAI 11384, MAI 66979, MAI 711110, MAI 711325, MAI 711326, MAI 838620, and MAI 965238

Section 1R15: Operability Evaluations (71111.15)

Photograph of boric acid deposits on containment spray pump 2P-35B

Condition Reports

CRs ANO-1-2004-0104, -00980, -01373; CRs ANO-2-2004-0065, -0253, -0406, -0420, -0446,

-0472, -0597, -0671, -0694, and -0722; and CR ANO-C-2002-00596

Procedures

1104.002, "Makeup & Purification System Operation," Supplement 3, "HPI Pump P-36A Test,"

Change 057-04-0

1104.005, "Reactor Building Spray System Operation," Supplement 3, "RB Spray Pump P-35A

Quarterly Test," Change 042-05-0

1107.002, "ES Electrical System Operation," Revision 19

1403.179, "Molded Case Breaker Testing," Revision 3

A-4 Attachment

Engineering Calculations

83-D-1034-03, Revision 0

97-E-0207-01, Revision 3

Section 1R17: Permanent Plant Modifications (71111.17)

V-SG-1-05, "Seismic Evaluation of Sluice Gate SG-1," Revision 1

V-SG-3-10, "MOV Torque Switch Setpoints," Revision 0

85-E-0118-01, "RB Penetration Overcurrent Protection Study," Revision 1

95-E-0059-01, "Amendment to RB Overcurrent Protection Study Calculation 85-E-0118-01,"

Change 0

Condition Reports

CRs ANO-1-2002-00280, -01646; -2004-00793, -01049, -01098, -01496; 2-1998-00334;

and -2004-00950

Drawings

15-FPC-5, "Spent Fuel Cooling Isometric," Revision 5

15-FPC-6, "Spent Fuel Cooling Isometric," Revision 6

MU-200, "Small Pipe Isometric Make-up Pump Discharge 2P-35A, B, & C Disch to 2E-26A & B,"

Revision 9

Engineering Requests

ERs ANO-1997-4783-002; -1998-0912-002, -1037-002; -1999-2143-007, -008; -2000-3258-002;

-2001-0541-001, -002, -1280-000; -2002-0271-000, -0528-005, and -0875-000

Procedures

1012.020, "Radioactive Material Control, "Revision 6

1052.022, "Radiological Effluents and Environmental Monitoring Program," Revision 2

6000.030, "Control of Installation," Revision 7

6010.001, "DCP Development," Revision 8

6010.003, "Limited Change Package and Plant Change Development," Revision 2

6030.005, "Control of Modification Work," Revision 6

6030.100, "Modification Implementation Procedure Program," Revision 4

A-5 Attachment

Section 1R19: Postmaintenance Testing (71111.19)

Procedures

1103.005, "Pressurizer Operation," Supplement 1, Change 030-04-0

1106.006, "Emergency Feedwater Pump Operation," Supplement 11, Change 064-03-0

1106.006, "Emergency Feedwater Pump Operation," Supplement 12, Change 064-03-0

2104.005, "Containment Spray," Supplement 1, Change 041-08-0

2104.036, "Emergency Diesel Generator Operations," Supplement 2A, Change 047-06-0

Section 1R22: Surveillance Testing (71111.22)

Procedures

1103.005, "Pressurizer Operation," Supplement 5, Change 030-04-0

1104.002, "Makeup & Purification System Operations," Supplement 5, Change 057-12-0

2104.029, "Service Water Systems Operations," Supplement 1B, Change 053-08-0

2104.036, "Emergency Diesel Generator Operations," Supplement 2A, Change 047-06-0

Work Order Packages

50689580 and MAI - 75944

Section 2OS1: Access Controls to Radiologically Significant Areas (IP 71121.01)

Radiation Work Permits

2004-1439, "Remove/Replace Plenum; Install/Remove Indexing Fixture"

2004-1442, "Remove/Replace Steam Generator Manways"

2004-1452, "Reactor Head Nozzle Repair Activities"

2004-1453, "Reactor Head Nozzle Inspection"

Procedures

1000.031, "Radiation Protection Manual," Change Notice 019-03-0

1012.017, "Radiological Posting and Entry/Exit," Change Notice 007-03-0

1012.018, "Administration of Radiological Surveys," Change Notice 006-03-0

RP-108, "Radiation Protection Posting," Revision 1, dated January 02, 2002

Condition Reports

CRs C-2003-00397, -00754, -00929; C-2004-00739; 1-2003-00515; 2-2003-01473, and -01643

Audits

QA-15-2003-RBS-1-Multi September 6 through November 19, 2003

QA-14-2004-ANO-1 January 5 through February 19, 2004

LO-ALO-2004-00011 February 23-27, 2004

QS 2003-ENS-017

A-6 Attachment

Section 4OA5: Other

Procedures

1104.036, "Emergency Diesel Generator Operations," Revision 41

1107.001, "Electrical System Operations," Revision 60

1015.008, "Unit 2 SDC Control," Revision 18

1015.033, "ANO Switchyard and Transformer Yard Controls," Revision 2

2104.036, "Emergency Diesel Generator Operations," Revision 47

2107.001, "Electrical System Operations," Revision 48

Forms

OPS-146, "Extended EDG Outage Coordinator Checklist" revision dated May 5, 2004

Miscellaneous

Maintenance Rule Database for Unit 1 and Unit 2 Main, Unit Auxiliary, and Startup Transformers

Videotapes associated with Procedure 2311.09, "Units 1 and 2 Alloy 600 Inspection," Revision 5,

on the review of reactor vessel lower head inspection

LIST OF ACRONYMS

ANO Arkansas Nuclear One

ASME American Society of Mechanical Engineers

CFR Code of Federal Regulations

CR condition report

CRDM control rod drive mechanism

ECCS emergency core cooling system

EDG emergency diesel generator

HPSI high pressure safety injection

kV kilovolt

LER licensee event report

LPSI low pressure safety injection

MOV motor-operated valve

MNSA mechanical nozzle seal assembly

MVA megavolt amp

NCV noncited violation

PI performance indicator

PI&R problem identification and resolution

QCST Q condensate storage tank

SSC structure, system, or component

TI temporary instruction

URI unresolved item

A-7 Attachment

Unit 2 Containment Spray Pump B

Boric Acid Deposits

A-8 Attachment