05000458/LER-1985-061, Corrected Ltr Forwarding LER 85-061-00.Tracking Number Changed to RBG-23041

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Corrected Ltr Forwarding LER 85-061-00.Tracking Number Changed to RBG-23041
ML20151U033
Person / Time
Site: River Bend Entergy icon.png
Issue date: 01/24/1986
From: Booker J
GULF STATES UTILITIES CO.
To:
NRC OFFICE OF ADMINISTRATION (ADM)
References
RBG-23041, NUDOCS 8602100445
Download: ML20151U033 (1)


LER-2085-061, Corrected Ltr Forwarding LER 85-061-00.Tracking Number Changed to RBG-23041
Event date:
Report date:
4582085061R00 - NRC Website

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arl GULF STATES UTILITIES COMPANY mivf R SEND STATION POST OmCE 60x 220 St FRANCISvtLLE. Louis 6ANA 70775 ARE A CODE 504 636-6094 346 6651 January 24, 1986

  • RBG- 23041 File Nos. G9.5, G9.25.1.3-U.S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555

Dear Sir:

River Bend Station - Unit 1 Docket No. 50-458 Please find enclosed Licensee Event Report No.85-061 for River-Bend Station - Unit 1. This report is submitted pursuant to 10CFR50.73.

Sincerely, J. E. Booker

[ Manager-Engineering, Nuclear Fuels & Licensing-River Bend Nuclear Group JEB/ FP /[EH/amg cc: U. S. Nuclear Regulatory Commission 611 Ryan Plaza, Suite 1000 Arlington, TX 76011 INPO Records Ce'ter n 1100 Circle 75 Parkway Atlanta, GA 30339-3064 8602100445 860124 I PDR ADOCK 05000458 S PDR

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On 12/25/85 at 1713, with the unit in operational condition 2 (startup) .and during the performance of a surveillance test procedure, a Reactor Water Cleanup (RWCU) system isolation occurred. The cause was attributed to an error in the surveillance test procedure. The performance of the procedure was terminated and the RWCU system was returned to service with no further problems occurring. The procedure was revised and successfully completed on 12/27/85. There wae no impact on the safe operation of the plant or the health and safety of the public since no identifiable leakage condition existed within the RWCU system.

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  • r 5:S i85 - Q6liff0,0 0,2c,o.3 On 12/25/85 at'1713 with the unit in operational condition 2 (startup), an inadvertent Reactor Water Cleanup (RWCU) (IEEE:CE) isolation occurred during the performance of Surveillance Test Procedure STP-207-4218 "RWCU System Isolation Differential Flow Timer Quarterly Channel Calibration." The isolation occurred during the placement of a test switch and was a result of an error contained in the procedure. The switch was removed and the performance of the surveillance test procedure was terminated. The

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RWCU system was returned to service with no further problems occurring.

Investigation revealed that the procedure failed to require switch E31-SlA (RWCU Bypass Switch) to be placed in the bypass position while connecting the required test equipment. As directed by the procedure, the Instrument & Controls technicians placed a test switch across terminals 9 and 10 on TB12 for temperature switch E31-N609A. These terminals are located immediately adjacent to each other. During the installation of the switch the connections were shorted causing the inadvertent isolation.

In an effort to prevent recurrence, Surveillance Test Procedure STP-207-4218 was revised per Temporary Change Notice 85-4487 to require switch E31-SlA to be placed in the bypass position prior to installing the required test equipment. As a result of an additional RWCU isolat' ion occurring during the performance of STP-207-4218 on 12/26/85 (reference LER 85-062) , other procedural

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RIVER BDID STATION o[stoIo[o1 4t 5, 8 ,l 8,5 _ 0,6 9 1h o O f f 0,3 !a, 0 , 3 errors were corrected per Temporary Change Notice 85-4911 and STP-2 7-4218 was successfully completed on 12/27/85.

There was no impact on the safe operation of the plant or the health and safety of the public since no identifiable leakage condition existed within the RWCU system.

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