03-07-2016 | On January 5, 2016, at 10:58 p.m. CST, with the plant operating at 100 percent power, the main control room alarm indicating high pressure in the auxiliary building actuated. Operators confirmed that the building pressure was out of specification. Secondary containment was declared inoperable, and the Division 2 standby gas treatment system was started. This action restored building pressure to the acceptable range, and secondary containment was declared operable at 12:27 a.m. on January 6. An inspection of the auxiliary building normal ventilation system found that discharge dampers on the exhaust fans were degraded, and the flow control damper on the supply fans was not operating correctly. In order to restore the normal ventilation system to service, the troubleshooting plan for this condition temporarily altered the operating configuration of the system to close the suction damper on the idle exhaust fan.
This prevents backflow through the idle fan, allowing the system to control building pressure within the required operating range.
Corrective maintenance is being planned to restore the material condition of the normal ventilation system. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(v)(C) as an event that caused the secondary containment to be potentially incapable of performing its safety function. , |
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Category:Letter
MONTHYEARIR 05000458/20230402024-01-18018 January 2024 95001 Supplemental Inspection Supplemental Report 05000458/2023040 and Follow-Up Assessment Letter RBG-48271, Supplement to License Amendment Request to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times RITSTF Initiative 4b and Application to Adopt 10 CFR 50.69, Risk2024-01-12012 January 2024 Supplement to License Amendment Request to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times RITSTF Initiative 4b and Application to Adopt 10 CFR 50.69, Risk ML24012A1962024-01-12012 January 2024 Response to 2nd Round Request for Additional Information Concerning Relief Request Number EN-RR-22-001 Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and ML24011A1742024-01-11011 January 2024 Security Baseline Inspection Report (Cover Letter) ML23349A1672023-12-21021 December 2023 Request for Withholding Information from Public Disclosure ML23348A3572023-12-14014 December 2023 Application to Revise Technical Specifications to Use Online Monitoring Methodology Slides and Affidavit for Pre-Submittal Meeting ML23340A1592023-12-13013 December 2023 Entergy Operations, Inc. - Entergy Fleet Project Manager Assignment ML23352A0292023-12-13013 December 2023 Entergy - 2024 Nuclear Energy Liability Evidence of Financial Protection IR 05000458/20230102023-12-12012 December 2023 Biennial Problem Identification and Resolution Inspection Report 05000458/2023010 RBG-48267, Reply to a Notice of Violation, NRC Inspection Report 05000458/20230032023-12-0707 December 2023 Reply to a Notice of Violation, NRC Inspection Report 05000458/2023003 ML23333A1362023-11-29029 November 2023 Supplement to Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23325A1432023-11-21021 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23310A0322023-11-13013 November 2023 Integrated Inspection Report 05000458/2023003 IR 05000458/20230032023-11-13013 November 2023 Integrated Inspection Report 05000458/2023003 ML23311A2082023-11-0909 November 2023 Reassignment of U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch IV ML23311A4322023-11-0909 November 2023 Notification of NRC Supplemental Inspection (95001) and Request for Information RBG-48264, Core Operating Limits Report (COLR) - Cycle 23, Revision 12023-11-0606 November 2023 Core Operating Limits Report (COLR) - Cycle 23, Revision 1 RBG-48260, Notification of Readiness for Supplemental Inspection2023-10-12012 October 2023 Notification of Readiness for Supplemental Inspection ML23278A2402023-10-0606 October 2023 Regulatory Audit Plan in Support of License Amendment Requests to Revise TSs to Adopt Risk-Informed Completion Times and Implement the Provisions of 10 CFR 50.69 RBG-48258, Notification of Readiness for Supplemental Inspection2023-10-0505 October 2023 Notification of Readiness for Supplemental Inspection RBG-48259, Revision to Reply to Notice of Violation; EA-23-0552023-10-0303 October 2023 Revision to Reply to Notice of Violation; EA-23-055 ML23270B9932023-09-29029 September 2023 Request to Update ASME Boiler & Pressure Vessel Code Relief Request SE with NRC-Approved Revision of Bwrip Guidelines (GG-ISI-020 & RBS-ISI-019) (EPID L-2022-LLR-0090) - Non-Proprietary ML23269A1242023-09-27027 September 2023 Request for Withholding Information from Public Disclosure IR 05000458/20234012023-09-26026 September 2023 Cyber Security Inspection Report 05000458/2023401 IR 05000458/20230012023-09-21021 September 2023 NRC Inspection Report 05000458/2023001, Disputed Non-Cited Violation Rescinded RBG-48254, Report of Changes and Errors to 10CFR50.462023-09-21021 September 2023 Report of Changes and Errors to 10CFR50.46 IR 05000458/20234032023-09-21021 September 2023 NRC Security Inspection Report 05000458/2023403 (Cover Letter) RBG-48249, Reply to a Notice of Violation, EA-23-0712023-09-14014 September 2023 Reply to a Notice of Violation, EA-23-071 RBG-48253, Submittal of Owner'S Activity Report Form for Cycle 222023-09-12012 September 2023 Submittal of Owner'S Activity Report Form for Cycle 22 IR 05000458/20230122023-09-0101 September 2023 Comprehensive Engineering Team Inspection Report 05000458/2023012 IR 05000458/20230052023-08-21021 August 2023 Updated Inspection Plan for River Bend Station (Report 05000458/2023005) - Mid Cycle Letter RBG-48247, Reply to Notice of Violation; EA-23-0552023-08-21021 August 2023 Reply to Notice of Violation; EA-23-055 IR 05000458/20230922023-08-15015 August 2023 Final Significance Determination of a White Finding, Notice of Violation, and Follow-Up Assessment Letter; NRC Inspection Report 05000458/2023092 IR 05000458/20230022023-08-0909 August 2023 Integrated Inspection Report 05000458/2023002 ML23208A2112023-07-27027 July 2023 Entergy Operations Inc., Application to Revise Technical Specifications to Adopt TSTF-205, Revision of Channel Calibration, Channel Functional Test, and Related Definitions ML23195A0692023-07-24024 July 2023 2023 River Bend Station Notification of Biennial Problem Identification and Resolution Inspection and Request for Information IR 05000458/20230912023-07-20020 July 2023 Final Significance Determination of a White Finding, Notice of Violation, and Follow-Up Assessment Letter; NRC Inspection Report 05000458/2023091 ML23207A0762023-07-14014 July 2023 EN 56557 - Update to Part 21 Report Re Potential Defect with Trane External Auto/Stop Emergency Stop Relay Card Pn: XI2650728-06 ML23195A0222023-07-11011 July 2023 4-2022-012 Letter - OI Closure to Licensee IR 05000458/20234042023-07-11011 July 2023 NRC Security Inspection Report 05000458/2023404 (Cover Letter Only) IR 05000458/20230902023-06-26026 June 2023 NRC Inspection Report 05000458/2023090 and Preliminary White Finding ML23159A2302023-06-0808 June 2023 Response to Request for Additional Information Concerning Request to Update ASME Code Relief Request Safety Evaluations with NRC-Approved Revision of BWRVIP Guidelines (GG-ISI-020, and RBS-ISI-019) ML23159A0052023-06-0505 June 2023 56557-EN 56557 - Paragon - Redlined RBG-48226, Core Operating Limits Report (COLR) - Cycle 23, Revision 02023-05-31031 May 2023 Core Operating Limits Report (COLR) - Cycle 23, Revision 0 RBG-48237, Response to NRC Integrated Inspection Report 05000458/20230012023-05-25025 May 2023 Response to NRC Integrated Inspection Report 05000458/2023001 ML23130A2732023-05-10010 May 2023 and Waterford 3 Steam Electric Station - Response to Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations ML23117A2172023-05-0101 May 2023 Safety Evaluation for Quality Assurance Program Manual Reduction in Commitment ML23116A2352023-05-0101 May 2023 Integrated Inspection Report 05000458/2023001 RBG-48220, Submittal of 2022 Annual Radioactive Effluent Release Report2023-04-25025 April 2023 Submittal of 2022 Annual Radioactive Effluent Release Report 2024-01-18
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000458/LER-2017-0092017-11-13013 November 2017 Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door, LER 17-009-00 for River Bend, Unit 1 Regarding Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door 05000458/LER-2017-0072017-08-21021 August 2017 Automatic Reactor Scram due to Failure of Main Generator Voltage Regulator Mode Transfer Relay, LER 17-007-00 for River Bend Station - Unit 1 Regarding Automatic Reactor Scram due to Failure of Main Generator Voltage Regulator Mode Transfer Relay 05000458/LER-2017-0062017-07-13013 July 2017 Potential Loss of Safety Function of Onsite Power Sources due to Inadvertent Inoperability of Control Building Chiller, LER 17-006-00 for River Bend, Unit 1 re Potential Loss of Safety Function of Onsite Power Sources due to Inoperability of Control Building Chiller 05000458/LER-2016-0032017-06-0808 June 2017 Operations Prohibited by Technical Specifications Due to Reactor Control Rod Drift During Core Alterations, LER 16-003-01 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Control Blade Drift During Core Alterations 05000458/LER-2017-0052017-06-0505 June 2017 1 OF 3, LER 17-005-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Inoperable Main Control Room Filter Train 05000458/LER-2017-0042017-05-22022 May 2017 Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve, LER 17-004-00 for River Bend Station, Unit 1, Regarding Loss of High Pressure Core Spray Safety Function During Surveillance Due to Malfunction of Test Return Valve 05000458/LER-2017-0032017-05-0909 May 2017 Manual Reactor Scram Initiated in Response to Increase in Steam Pressure During Steam Leak Troubleshooting, LER 17-003-00 for River Bend Station, Unit 1, Regarding Manual Reactor Scram Initiated in Response to Increase in Steam Pressure During Steam Leak Troubleshooting 05000458/LER-2017-0022017-04-18018 April 2017 Loss of Safety Function of Onsite Electrical Distribution Due to Malfunction of Control Building HVAC System, LER 17-002-00 for River Bend Station, Unit 1, Regarding Loss of Safety Function of Onsite Electrical Distribution Due to Malfunction of Control Building HVAC System 05000458/LER-2017-0012017-04-0303 April 2017 Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open), LER 17-001-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications (Conduct of Operations With a Potential to Drain the Reactor Vessel With Primary Containment Open) 05000458/LER-2016-0072016-07-25025 July 2016 1 Operations Prohibited by Technical Specifications Due to Failure to Implement Required Actions Within Completion Time, LER 16-007-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Failure to Implement Required Actions Within Completion Time 05000458/LER-2016-0062016-07-12012 July 2016 Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers, LER 16-006-00 for River Bend Station re: Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers 05000458/LER-2016-0042016-03-29029 March 2016 Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power, LER 16-004-00 for River Bend, Unit 1, Regarding Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power 05000458/LER-2016-0022016-03-0707 March 2016 Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient, LER 16-002-00 for River Bend, Unit 1, Regarding Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient 05000458/LER-2016-0012016-03-0707 March 2016 Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System, LER 16-001-00 for River Bend, Unit 1, Regarding Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System 05000458/LER-2015-0102016-02-0808 February 2016 Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller, LER 15-010-00 for River Bend Station, Unit 1, Regarding Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller 05000458/LER-2015-0092016-01-26026 January 2016 1 OF 3, LER 15-009-00 for River Bend Station, Unit 1 Regarding Automatic Reactor Scram Due to Partial Loss of Offsite Power Caused by Fault in Local 230K Switchyard 05000458/LER-2015-0082016-01-18018 January 2016 Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller, LER 15-008-00 of River Bend Station, Unit 1, Regarding Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller 05000458/LER-2015-0072016-01-18018 January 2016 Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller, LER 15-007-00 for River Bend Station - Unit 1 Regarding Potential Loss of Safety Function of High Pressure Core Spray Due to Failure of Main Control Building Ventilation Chiller RBG-47473, Special Report for NEI 07-07 Notification2014-06-0404 June 2014 Special Report for NEI 07-07 Notification ML0627100382006-05-16016 May 2006 Final Precursor Analysis - River Bend Station, LER-458/04-005-01, Automatic Reactor Trip Due to Loss of Non-Vital 120V Instrument Bus 2017-08-21
[Table view] |
Reported lessons learned are incorporated into the licensing prociss and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
REPORTED CONDITION
On January 5, 2016, at 10:58 p.m. CST, with the plant operating at 100 percent power, the main control room alarm indicating high pressure in the auxiliary building [NF] actuated. Operators confirmed that the building pressure was out of specification. Secondary containment was declared inoperable, and the Division 2 standby gas treatment system [BI-1] was started. This action restored building pressure to the acceptable range, and secondary containment was declared operable at 12:27 a.m. on January 6. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that caused the secondary containment to be potentially incapable of performing its safety function.
BACKGROUND
The normal auxiliary building ventilation system [VF] is non-safety related, and comprises two 100 percent capacity supply fans, two 100 percent capacity exhaust fans, and the associated ductwork, dampers, and controls. A supply fan operates continuously, drawing air from outside and distributing it throughout the building. The supply fan discharge,dampers modulate automatically to maintain air flow at a nominal 10,000 standard cubic feet per minute. An exhaust fan continuously draws air from the building and expels it outside. The arrangement of the flow path through the building general equipment areas and pump rooms is balanced such that the system acts to maintain the building at a negative pressure.
During design-basis accident conditions, the auxiliary building is maintained at negative pressure by the standby gas treatment system.
That is a safety-related system that actuates automatically in response to certain plant parameters.
INVESTIGATION and IMMEDIATE ACTIONS The normal ventilation system was inspected, and it was determined that a combination of degraded components caused the condition:
- Seals on the exhaust fan (**FAN**) discharge damper (**BDMP**) vanes were degraded. This allowed air to flow backwards through the idle exhaust fan, causing the total exhaust outflow to decrease and building pressure to increase:
- The flow controller for the supply fan modulating dampers (**CDMP**) had failed, allowing excessive air flow that caused building pressure to increase.
In order to restore the normal ventilation system to service, the troubleshooting plan for this condition temporarily altered the operating configuration of the system to close the suction damper on the idle exhaust fan. This prevents backflow through the idle fan, allowing the system to control building pressure within the required operating range.
CORRECTIVE ACTION TO PREVENT RECURRENCE
Corrective maintenance is being planned to (1) replace the seals in the exhaust fan discharge dampers to eliminate the backflow path, and (2) calibrate the supply fan modulating damper control circuit.
PREVIOUS OCCURRENCE EVALUATION
No similar events have been reported by River Bend Station in the last three years.
SAFETY SIGNIFICANCE
The River Bend Updated Safety Analysis Report describes the sequence of events postulated to occur following a loss of coolant accident (LOCA). Part of that analysis is a projection of the maximum radiation dose received by a person at the site boundary. The LOCA dose calculation assumes that the standby gas treatment system is initiated 20 minutes into the event, and that secondary containment is at the required negative pressure within 30 minutes, such that filtration may be credited. As such, the safety function of secondary containment is maintained as long as the auxiliary building pressure is capable of being established within 30 minutes of the onset of the event. Since the ability of the standby gas treatment system to control building pressure within specifications under accident conditions was' demonstrated in the recovery from this condition, no loss of the safety function of secondary containment actually occurred. This event was, thus, of minimal significance to the health and safety of the public.
(NOTE: Energy Industry Identification System component function identifier and system name of each component or system referred to in the LER are annotated as (**XX**) and [XX], respectively.)
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05000458/LER-2016-001 | Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System LER 16-001-00 for River Bend, Unit 1, Regarding Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000458/LER-2016-002 | Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient LER 16-002-00 for River Bend, Unit 1, Regarding Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000458/LER-2016-003 | Operations Prohibited by Technical Specifications Due to Reactor Control Rod Drift During Core Alterations LER 16-003-01 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Control Blade Drift During Core Alterations | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000458/LER-2016-004 | Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power LER 16-004-00 for River Bend, Unit 1, Regarding Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000458/LER-2016-005 | Potential Loss of Safety Function of Onsite AC Sources and Operations Prohibited by Technical Specifications Due to Uncorrected Circuit Breaker Control Logic Design Causing Intermittent Failure to Close | | 05000458/LER-2016-006 | Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers LER 16-006-00 for River Bend Station re: Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000458/LER-2016-007 | 1 Operations Prohibited by Technical Specifications Due to Failure to Implement Required Actions Within Completion Time LER 16-007-00 for River Bend Station, Unit 1, Regarding Operations Prohibited by Technical Specifications Due to Failure to Implement Required Actions Within Completion Time | |
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