05000311/LER-1982-027, Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State

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Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State
ML20066A204
Person / Time
Site: Salem PSEG icon.png
Issue date: 10/20/1982
From: Heller R
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20066A199 List:
References
LER-82-027-03X, LER-82-27-3X, NUDOCS 8211050126
Download: ML20066A204 (1)


LER-2082-027, Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State
Event date:
Report date:
3112082027R00 - NRC Website

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UCENSEE EVENT REPORT CONTROL BLOCK: l l l l l .lh (PLE ASE PRINT CR TYPE alt CE!Ul:E3 INFORMATION) o i i 8 lN 9 l LICENSEE J l S lG CODE lS l 2 l@16 ol ol LICENSE le -l 0l O! 0l 0l Ol -l 260l 0l@l NUMsER 26 4 l 1lTYPE LICENSE 1lJO1l 1l@l l lg 67 CAT 68 CON'T O t 7 8 f y Q @SGl St 0l SlDOCKET 0l 0l Ol 3l ll88t hl99 0 l4EVENT NUMSER l1 DATE l8 l8 l2 gl 1l 0lREPORT 74 76 2l DATE 0l 8l 280 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 lon April 18, 1982, during routine power escalations the Control Room Operator informed g o lthe Shift Supervisor'that the Reactor Coolant System (RCS) Water Inventory o 4 ISP(0)4.4.7.2.d had not been performed within the time interval of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> pluf 25% g o 5 l required by the Technical Specifications. Steady state conditions, which are required g 10 ls l lfor performance of the surveillance, could not be obtained due to changes in Xenon g O 7 l reactivity. This occurrence constituted operation in a degraded mode in accordance y o8 lwith Technical Specification 6.9.1.9.b. g

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1 O l Surveillance of the containment sump pump and of the containment radioactivity monitors g g lwas increased, and RCS leakage was demonstrated to be within Specification limits.

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, 7 lThe RCS water inventory was performed, and at 0135 hours0.00156 days <br />0.0375 hours <br />2.232143e-4 weeks <br />5.13675e-5 months <br />, April 20, 1982, Action State ,

t 3 l ment 3.4.7.2.a was terminated. License Change Request 82-14 was submitted to eliminateg i 4 l the RCS water inventory requirement during non-steady state operation.

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