ML17328A400

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Responds to 900725 Ltr Re Commitments Made in Response to Generic Ltr 88-14 on Instrument Air Supply Problems Affecting safety-related Equipment.Simulator Training to Be Provided as Stated
ML17328A400
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/24/1990
From: ALEXICH M P
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: MURLEY T E
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1075B, GL-88-14, NUDOCS 9008300225
Download: ML17328A400 (5)


Text

ACCELERATED DISTBJBUTION DEMONSTPWTION SYSTEM REGULATORY INFORMATION DISTRIBUTION YSTEM (RIDS)'A!CESSION NBR:9008300225 DOC.DATE: 90/08/24 NOTARIZED:

NO DOCKET FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana&05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana&05000316 AUTH.NAME AUTHOR AFFILIATION ALEXICH,M.P.

Indiana Michigan Power Co.(formerly Indiana&Michigan Ele RECIP.NAME RECIPIENT AFFILIATION MURLEY,T.E.

'ocument Control Branch (Document Control Desk)

SUBJECT:

Responds to 900725 ltr re'commitments madee in response to Generic ltr 88-014.DISTRIBUTION CODE: R048D COPIES RECEIVED:LTR 1 ENCL 0 SIZE: TITLE: OR/Licensing Submittal:

Equipment Qualification NOTES: RECIPIENT ID CODE/NAME PD3-1 LA COLBURN,T.

INTERNAL: NRR/DET/EMEB 9H OC/LFMB ILE 01 EXTERNAL: LPDR NSIC COPIES LTTR ENCL RECIPIENT ID CODE/NAME PD3-1 PD NRR/DET/ESGB 8D OGC/HDS1'RES/DSIR/EIB NRC PDR COPIES LTTR ENCL NOTE TO ALL"RIDS" RECIPIENTS'LEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 12 ENCL ff II I If I~~I

~~'r.~~Indiana Michigan Power Company P.O.Box 16631 Columbus, OH 43216 IINWAHA S~HCNE6'$!M PQWM AEP:NRC:1075B Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 INSTRUMENT AIR SUPPLY PROBLEMS AFFECTING SAFETY-RELATED EQUIPMENT (NRC Generic Letter 88-14)U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Attn: T.E.Murley August 24, 1990

Dear Dr.Murley:

The purpose of this letter is to provide a response to your letter of July 25, 1990 regarding commitments we had made in response to Generic Letter 88-14.Specifically, it was requested that we confirm the staff's understanding of two commitments that had been made in our letters of February 24, 1989 (AEP:NRC:1075) and March 23, 1989 (AEP:NRC:1075A).

The two commitments identified in your letter and our response to each are as follows: (1)NRC Position"You have committed to establish a formal air dryer performance monitoring program from the informal procedure being developed at the time of your initial response.This program is intended to change the emphasis of your program from acceptance testing toward reliability enhancement." Comment We confirm our agreement with the above statement.

O."029 9008300225 900824 PDR ADQCK 05000315 P FNU Dr.T.E.Murley-2-AEP:NRC:1075B (2)NRC Position"You have stated that simulator training incorporating loss-of-air scenarios was to be supplied to all licensed and non-licensed plant operators beginning in 1989.This training is intended to supplement classroom training begun in 1988." Comment The intent of our statement is that we will provide simulator training to all licensed operators under the requalification program and as part of our replacement program to non-licensed operators preparing to take the NRC licensing examination.

We affirm that we will provide simulator training as described under item (2)below.Based on is given our commitments, the status of these two program upgrades below for your information:

Air Dr er Performance Monitorin Pro ram Indiana Michigan Power, Donald C.Cook Nuclear Plant procedure+*12 THP 6040 PER.005,"Control Air Performance Tests," Revision 4, was revised on June 1, 1989 to establish a performance monitoring program.Revision 5, under the new title"Control Air Performance Monitoring" changed the focus of the previous revision from performing required maintenance to coordinating needed preventative maintenance through MHI 5030,"Preventative Maintenance and Environmental Qualification Program," by documentation and inspection during routine tours.These changes were also made in accordance with recommendations of INPO SOER 88-01.(2)0 erator Simulator Trainin Incor oratin Loss-of Air Scenarios As part of our licensed operator requalification program, Lessen Plan RQ-S-1474,"Loss of Plant/Control Air," was first conducted during a requalification training cycle beginning on October 12, 1989.This included simulator training on a partial and complete loss of plant and control air.The loss-of-air simulator scenarios are also planned for the training cycle beginning on November 26, 1990.Additional simulator training for licensed operators will be determined based on a needs analysis.

~~0~~0~\Dr.T.E.Murley-3-AEP:NRC:1075B Lesson Plan RO-S-0702,"Loss of Plant/Control Air, PTS," was presented to our licensed operator replacement class (non-licensed operators preparing to take the NRC licensing exam)during the period April 11 through April 25, 1989, and is a regular part of our replacement program.This lesson plan also includes simulator training on a partial and complete loss of plant and control air.Please note that non-licensed operators do no receive simulator training unless enrolled in a replacement class.This document has been prepared following Corporate procedures that incorporate a reasonable set of controls to ensure its accuracy and completeness prior to signature by the undersigned.

Sincerely, M.P.Al xich Vice President dfw cc: D.H.Williams, Jr.A.A.Blind-Bridgman J.R.Padgett G.Charnoff A.B.Davis-Region III NRC Resident Inspector-Bridgman NFEM Section Chief