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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20042F3541990-04-30030 April 1990 Special Rept Re Failure to Prevent Performance Degradation of Reactor Bldg Cooling Units.Caused by Mgt Deficiency & Inadequate Program.Cooling Unit Declared Inoperable & Removed from Svc for Cleaning & Placed Back in Operation ML20024C4181983-07-0101 July 1983 Ro:On 830525,fire Barrier Penetrations Found Nonfunctional. Caused by Design Deficiency.Fire Watch Posted,Penetrations Repaired & Procedures Revised ML20024C1271983-07-0101 July 1983 Ro:On 830623,visual Insp Revealed Three Broken Holddown Springs.Investigation Incomplete.Ro 269/83-13 Will Be Submitted by 830721 ML20024C4141983-06-29029 June 1983 Ro:On 830509 & 12,fire Barrier Smoke Exhaust Penetrations 3-K-5-2,3-C-5-3 & 4 Found W/O Seal & 3-C-5-3 Did Not Have Fusible Damper,Respectively.Caused by Inadequate Info & Insufficient Guidance Provided by Design Engineering ML20023B6511983-04-29029 April 1983 ROs 269/83-10 & 287/83-04 Re 821212 & 830303 Loss of Containment Integrity.Mgt Audit in Progress.Summary List of Completed & Remaining Activities,W/Projected Completion Dates,Encl ML20027B8581982-09-21021 September 1982 Ro:Advising That 820820 Occurrence Involving Loss of Electric Power to Valve CCW-8 Determined Not Reportable. Operability of Valve Demonstrated.No Further Action Required ML20027B7691982-09-16016 September 1982 RO 269/82-14:investigation Re Reactor Bldg Penetrations That May Not Have Been Leak Rate Tested Incomplete.Rept to Be Submitted by 820930 ML20052A3291982-04-0909 April 1982 Informs That Review Per RO-269/82-07 Has Determined That Plant Design & Const Predate Std Re Westinghouse SAI-1 Type Relays Not Meeting Full Surge Requirements ML20052A4261982-04-0202 April 1982 RO 269/82-06:on 820306,steam Generator 1B Indicated Tube Leak of 0.08 Gpm.Incident Under Investigation.Next Rept Expected by 820416 ML20050A9751982-03-12012 March 1982 RO 287/82-04:on 820226,3A2 HPI Normal Makeup Nozzle Found to Have Broken Thermal Sleeve Tack Welds.Investigation Revealed Cracks in Safe End & Upstream Piping.Next Rept Expected by 820409 ML20049J5541982-02-25025 February 1982 Ro:Advising of Delay Until 820311 to Provide Complete Rept of RO-281/82-03 Re Steam Generator Tube Leak ML20040F7611982-02-0505 February 1982 Ro:On 820122,during Visual Insp of Core Barrel Assembly, Thermal Shield & Shock Pad Bolts Found Broken & Shock Pad Was Skewed.Thermal Shock Bolts to Be Replaced.Loosened Shock Pad Evaluation Underway ML20040E6871982-01-28028 January 1982 RO 269/81-50:on 811229,reactor Bldg Cooling Unit C Declared Inoperable Due to Inability to Open Discharge Valve 1LPSW-24.Investigation & Rept Expected to Be Completed by 820211 ML20040C8421982-01-0808 January 1982 Suppl 3 to RO 269/81-11:re Broken Lower Thermal Shield Bolts.Caused by Intergranular Stress Corrosion Cracking in Region of Pronounced Microstructure Transition at head-to-shank Fillet.Bolts Replaced.Drawings Encl ML20011A7231981-10-21021 October 1981 Ro:On 811019,four Liquid Waste Releases Were Made W/O Adequate Sampling.Caused by Failure to Make Change to Sample Point.Procedure Revised to Specify Correct Sampling Point for Sys Configuration ML20010F6791981-09-0404 September 1981 RO 270/81-14:on 810821,2A1 Reactor Coolant Pump Electrical Penetration Was Discovered Depressurized & Could Not Be Repressurized w/SF6 Gas.Cause Not Stated.Investigation & Complete Rept Will Be Sent by 810918 ML20038C8171981-08-25025 August 1981 Ro:On 810814,tritium Concentrations in Downstream Water Samples Exceeded Tech Spec Control Level for Second Quarter of 1981.Analysis of Max Dose Estimates Concluded That Concentrations Will Not Adversely Affect Public Health ML20010A8721981-08-0505 August 1981 RO 269/81-11,Suppl 1:on 810715,core Barrel Assembly Thermal Shield Bolts Found Broken.Cause Not Stated.Search for Loose Parts Turned Up All Missing Thermal Shield Parts Except for One Thermal Shield Bolt Head.Investigation Continuing ML20009E7351981-07-28028 July 1981 Ro:On 810717,fire Suppression Water Sys Found Inoperable. Caused by Open Main Control Source Breakers.Breakers Closed & Sys Successfully Tested ML20038C8031981-07-0606 July 1981 Ro:On 810210,radioactivity Levels of Aquatic Vegetation Samples Exceeded Control Level by Greater than 50 Times.Info Supersedes 810225 Submittal ML20009F4311981-07-0101 July 1981 Ro:On 810630,during Performance of Normal Power Procedure, Backup Function of Units Isolating & Transfer Diodes on 125 Volt Dc Instrumentation & Control Sys Was Observed. Proposed Tech Spec Change Will Be Submitted ML20009H2701981-04-0101 April 1981 RO:810319 Determination Declaring Portions of Low Power Injection Sys Seismically Inoperable Was Premature.Hanger Noncomformance Repaired within 48-h Per IE Bulletin 79-14. Item Not Reportable Per Tech Spec 6.6.2.1a(9) ML20005A8771981-02-25025 February 1981 Ro:On 810219 Analytical Results of Aquatic Vegetation Samples Collected on 810210 Indicated That Radioactivity Levels Exceeded Tech Specs.Cause Not Stated ML19282D0291979-01-15015 January 1979 RO 269/7827 on 781214:on 781213,reactor Coolant Temp Became Erratic.Feedwater Problem Resulted from Operation of One or More Feedwater Valves.Power Cords Have Been Fitted ML19263C9841978-11-30030 November 1978 RO 270/78-12 on 781105:stop Check Valve from 2AHPI Pump to 2A12C Pump Closed During Flow Test.Valve Was Opened & Check Valve Functional Test Completed ML19316A3701978-06-0505 June 1978 RO 269/78-13:on 780427,primary-to-secondary Leak in 1B Steam Generator Occurred.Caused by Tube Leaks.Tube 69-1 Had Weld Crack.Tube 74-2 Had Circumferential Crack.Cracked & Suspect Tubes explosive-plugged.Investigation Continuing ML19312C2361978-04-21021 April 1978 RO-269/78-07 & 09:on 780314 & 22,field Flashing Breaker Found Inoperable.Cause for Repeated Inoperability Has Not Been Determined.Faulty Relays Replaced Before 780322 Failure.Recorder Will Be Installed to Monitor Trip Circuits ML19316A3811978-04-11011 April 1978 RO 269/78-08:on 780315,valve FDW-108 Failed to Close.Failure Has Occurred Previously.Caused by Apparent Unsuitability of Valves for long-term Operation in Sys Environ.Valve Stem Lubricated.Valves Will Be Replaced ML19316A4041978-04-0707 April 1978 RO 269/78-06:on 780310,field Flashing Breaker Failed to Close During Startup of Keowee Hydro Unit 2.Breakers & Associated Relays Checked.Circuits Checked.Cause of Breaker Malfunction Unknown.Search for Possible Causes Continues ML19316A3891978-04-0707 April 1978 RO 269/78-10:on 780323,Unit 2 Not Verified Operable within Time Limit.Caused by Personnel Error.Station Procedure, Removal & Restoration of Equipment, Not Properly Used. Personnel Instructed by Operating Engineer ML19308A7531978-03-23023 March 1978 RO 269/78-03:on 780222,Unit 2 Field Flashing Breaker Failed to Close.Cause of Breaker Malfunction Not Determined.Relays in Breaker Control Circuit Were Replaced.Investigation to Control Breaker Sys Faults Continues ML19316A4641978-03-15015 March 1978 RO 269/78-04:on 780301,two Reactor Bldg Cooling Units Found Inoperable Simultaneously.Caused by Insufficient Installation Procedures Allowing Trip Point to Be Set Too Low.Breaker Reset & Trip Setpoint Increased ML19316A4171978-02-0303 February 1978 RO 269/78-01:on 780203,field Flashing Breaker Failed to Close.Controls Checked & Found in Proper Condition.Breaker Checked & Cleaned.Cause of Failure Not Determined ML19317F3461978-02-0202 February 1978 RO 270/78-04:on 780202,nuclear Instruments Found Out of Calibr in Less Conservative Direction & Could Have Prevented Fulfillment of Functional Requirements of Reactor Protective Sys.Cause Not Stated.Administrative Measures Taken ML19308A7971978-01-31031 January 1978 RO 269/78-02:on 780105,Keowee Hydro Unit 1 Not Verified Operable within 1-h of Taking Keowee Unit 2 Out of Svc. Caused by Failure to Follow Established Procedures by Personnel.Operators Instructed in Tech Specs ML19317E0451978-01-26026 January 1978 RO 269/77-31:on 771229,leakage of Less than 1 Gallon Per Minute Noted.Caused by Failure of Switch 1PS-364 Diaphragm. Switch 1PS-364 to Be Replaced During Future outage.1PT-21P Switch Recalibr & Returned to Svc ML19316A4841978-01-19019 January 1978 RO 269/77-30:on 771220,primary Leak Through Pressurizer Spray Bypass Valve RC-2 Indicated.Caused by Packing Leak on Pressurizer Spray Bypass Valve.Valve RC-2 Repacked & Tested for Leaks ML19317D9631978-01-18018 January 1978 Incident Investigation Rept RO-B-692:on 780117,Keowee Unit 2 Removed from Svc for Maint & Keowee Unit 1 Not Verified Operable within 1-h Per Tech Specs.Keowee Unit 1 Verified Operable Upon Discovery ML19308A7841978-01-18018 January 1978 RO 269/77-29:on 771219,Keowee Hydro Unit 2 Failed to Start on Initiation from Oconee Control Room.Field Flashing Breaker Failed to Close.Cause Not Determined.Breaker Inspected & Serviced & Found Operable ML19317D9591978-01-13013 January 1978 Incident Investigation Rept RO-B-690:on 780113,indications Reading High During Calibr on a Core Flood Tank (IP/0/A/020/01A).Error May Have Allowed Unit Operation in Violation of Tech Specs 3.3.3 ML19317D8781977-12-19019 December 1977 RO 269/77-28:on 771216,B&W Discovered Min Vol & Concentration Requirements Were Insufficient for Reactor Shutdown.Cause Not Given.Boron Solution Vol Increased to Provide Adequate Margin for Shutdown ML19308B1701977-12-15015 December 1977 RO 269/77-27:on 771215,B&W Discovered Error in Computer Used for Incore Detector Signal Processing.Initial Action to Reduce Positive Imbalance Trip Setpoints by 2.5% ML19317F2651977-12-0606 December 1977 Ro:On 771206,valve 3LP-28 Not Locked Open as Required by Tech Specs.Valve Locked Open Upon Discovery.Forwards Util Incident Investigation Rept B-674 ML19308A8451977-11-10010 November 1977 Ro:On 771107,analysis of Raw Water Supply Samples Collected in July,Aug & Sept 1977 Showed Tritium Concentration Exceeding Control Level by Greater than Ten Times ML19312C6131977-10-31031 October 1977 Ro:On 771026,milk Samples Collected 771005 Showed I-131 Concentrations Exceeded Control Levels Per Tech Specs Section 6.6.2.2.a.Higher Levels Attributed to 770917 Chinese Nuclear Test ML19312C7141977-09-26026 September 1977 Ro:On 770920,radionuclide (Cs-134 & Cs-137) Levels of Keowee River Sediment Samples Collected in Aug 1977 Registered 10 Times Control Level.Based on Diluted Tailrace Concentrations,Levels Lie within Expected Values ML19312C6251977-08-25025 August 1977 Ro:On 770819,fish Samples Collected During July 1977 Showed Cs-137 Levels Exceeding Control Limits by Over Ten Times. Concentrations within Health & Safety Limits & No Corrective Actions Planned ML19312C6181977-08-18018 August 1977 Ro:On 770812,composite Surface Water Samples Collected from Apr-June 1977 Showed Tritium Concentration Exceeding Control Level by 50 Times.No Threat to Public Safety & No Corrective Action Planned ML19317F3221977-08-16016 August 1977 RO 270/77-10:on 770803,reactor Bldg Purge & Penetration Room Ventilation Sys Running Time Check Revealed That Required Surveillance of Filter Sys Was Not Performed.Caused by Failure to Implement Adequate Administrative Procedures ML19317D9971977-08-16016 August 1977 RO 269/77-17A:on 770517,emergency Power Source Inadvertently Isolated.Caused by Procedural Inadequacy of Some Tests. Periodic Test Procedure Revised for Restoring Emergency Power Sys to Proper Lineup 1990-04-30
[Table view] Category:LER)
MONTHYEARML20042F3541990-04-30030 April 1990 Special Rept Re Failure to Prevent Performance Degradation of Reactor Bldg Cooling Units.Caused by Mgt Deficiency & Inadequate Program.Cooling Unit Declared Inoperable & Removed from Svc for Cleaning & Placed Back in Operation ML20024C4181983-07-0101 July 1983 Ro:On 830525,fire Barrier Penetrations Found Nonfunctional. Caused by Design Deficiency.Fire Watch Posted,Penetrations Repaired & Procedures Revised ML20024C1271983-07-0101 July 1983 Ro:On 830623,visual Insp Revealed Three Broken Holddown Springs.Investigation Incomplete.Ro 269/83-13 Will Be Submitted by 830721 ML20024C4141983-06-29029 June 1983 Ro:On 830509 & 12,fire Barrier Smoke Exhaust Penetrations 3-K-5-2,3-C-5-3 & 4 Found W/O Seal & 3-C-5-3 Did Not Have Fusible Damper,Respectively.Caused by Inadequate Info & Insufficient Guidance Provided by Design Engineering ML20023B6511983-04-29029 April 1983 ROs 269/83-10 & 287/83-04 Re 821212 & 830303 Loss of Containment Integrity.Mgt Audit in Progress.Summary List of Completed & Remaining Activities,W/Projected Completion Dates,Encl ML20027B8581982-09-21021 September 1982 Ro:Advising That 820820 Occurrence Involving Loss of Electric Power to Valve CCW-8 Determined Not Reportable. Operability of Valve Demonstrated.No Further Action Required ML20027B7691982-09-16016 September 1982 RO 269/82-14:investigation Re Reactor Bldg Penetrations That May Not Have Been Leak Rate Tested Incomplete.Rept to Be Submitted by 820930 ML20052A3291982-04-0909 April 1982 Informs That Review Per RO-269/82-07 Has Determined That Plant Design & Const Predate Std Re Westinghouse SAI-1 Type Relays Not Meeting Full Surge Requirements ML20052A4261982-04-0202 April 1982 RO 269/82-06:on 820306,steam Generator 1B Indicated Tube Leak of 0.08 Gpm.Incident Under Investigation.Next Rept Expected by 820416 ML20050A9751982-03-12012 March 1982 RO 287/82-04:on 820226,3A2 HPI Normal Makeup Nozzle Found to Have Broken Thermal Sleeve Tack Welds.Investigation Revealed Cracks in Safe End & Upstream Piping.Next Rept Expected by 820409 ML20049J5541982-02-25025 February 1982 Ro:Advising of Delay Until 820311 to Provide Complete Rept of RO-281/82-03 Re Steam Generator Tube Leak ML20040F7611982-02-0505 February 1982 Ro:On 820122,during Visual Insp of Core Barrel Assembly, Thermal Shield & Shock Pad Bolts Found Broken & Shock Pad Was Skewed.Thermal Shock Bolts to Be Replaced.Loosened Shock Pad Evaluation Underway ML20040E6871982-01-28028 January 1982 RO 269/81-50:on 811229,reactor Bldg Cooling Unit C Declared Inoperable Due to Inability to Open Discharge Valve 1LPSW-24.Investigation & Rept Expected to Be Completed by 820211 ML20040C8421982-01-0808 January 1982 Suppl 3 to RO 269/81-11:re Broken Lower Thermal Shield Bolts.Caused by Intergranular Stress Corrosion Cracking in Region of Pronounced Microstructure Transition at head-to-shank Fillet.Bolts Replaced.Drawings Encl ML20011A7231981-10-21021 October 1981 Ro:On 811019,four Liquid Waste Releases Were Made W/O Adequate Sampling.Caused by Failure to Make Change to Sample Point.Procedure Revised to Specify Correct Sampling Point for Sys Configuration ML20010F6791981-09-0404 September 1981 RO 270/81-14:on 810821,2A1 Reactor Coolant Pump Electrical Penetration Was Discovered Depressurized & Could Not Be Repressurized w/SF6 Gas.Cause Not Stated.Investigation & Complete Rept Will Be Sent by 810918 ML20038C8171981-08-25025 August 1981 Ro:On 810814,tritium Concentrations in Downstream Water Samples Exceeded Tech Spec Control Level for Second Quarter of 1981.Analysis of Max Dose Estimates Concluded That Concentrations Will Not Adversely Affect Public Health ML20010A8721981-08-0505 August 1981 RO 269/81-11,Suppl 1:on 810715,core Barrel Assembly Thermal Shield Bolts Found Broken.Cause Not Stated.Search for Loose Parts Turned Up All Missing Thermal Shield Parts Except for One Thermal Shield Bolt Head.Investigation Continuing ML20009E7351981-07-28028 July 1981 Ro:On 810717,fire Suppression Water Sys Found Inoperable. Caused by Open Main Control Source Breakers.Breakers Closed & Sys Successfully Tested ML20038C8031981-07-0606 July 1981 Ro:On 810210,radioactivity Levels of Aquatic Vegetation Samples Exceeded Control Level by Greater than 50 Times.Info Supersedes 810225 Submittal ML20009F4311981-07-0101 July 1981 Ro:On 810630,during Performance of Normal Power Procedure, Backup Function of Units Isolating & Transfer Diodes on 125 Volt Dc Instrumentation & Control Sys Was Observed. Proposed Tech Spec Change Will Be Submitted ML20009H2701981-04-0101 April 1981 RO:810319 Determination Declaring Portions of Low Power Injection Sys Seismically Inoperable Was Premature.Hanger Noncomformance Repaired within 48-h Per IE Bulletin 79-14. Item Not Reportable Per Tech Spec 6.6.2.1a(9) ML20005A8771981-02-25025 February 1981 Ro:On 810219 Analytical Results of Aquatic Vegetation Samples Collected on 810210 Indicated That Radioactivity Levels Exceeded Tech Specs.Cause Not Stated ML19282D0291979-01-15015 January 1979 RO 269/7827 on 781214:on 781213,reactor Coolant Temp Became Erratic.Feedwater Problem Resulted from Operation of One or More Feedwater Valves.Power Cords Have Been Fitted ML19263C9841978-11-30030 November 1978 RO 270/78-12 on 781105:stop Check Valve from 2AHPI Pump to 2A12C Pump Closed During Flow Test.Valve Was Opened & Check Valve Functional Test Completed ML19316A3701978-06-0505 June 1978 RO 269/78-13:on 780427,primary-to-secondary Leak in 1B Steam Generator Occurred.Caused by Tube Leaks.Tube 69-1 Had Weld Crack.Tube 74-2 Had Circumferential Crack.Cracked & Suspect Tubes explosive-plugged.Investigation Continuing ML19312C2361978-04-21021 April 1978 RO-269/78-07 & 09:on 780314 & 22,field Flashing Breaker Found Inoperable.Cause for Repeated Inoperability Has Not Been Determined.Faulty Relays Replaced Before 780322 Failure.Recorder Will Be Installed to Monitor Trip Circuits ML19316A3811978-04-11011 April 1978 RO 269/78-08:on 780315,valve FDW-108 Failed to Close.Failure Has Occurred Previously.Caused by Apparent Unsuitability of Valves for long-term Operation in Sys Environ.Valve Stem Lubricated.Valves Will Be Replaced ML19316A4041978-04-0707 April 1978 RO 269/78-06:on 780310,field Flashing Breaker Failed to Close During Startup of Keowee Hydro Unit 2.Breakers & Associated Relays Checked.Circuits Checked.Cause of Breaker Malfunction Unknown.Search for Possible Causes Continues ML19316A3891978-04-0707 April 1978 RO 269/78-10:on 780323,Unit 2 Not Verified Operable within Time Limit.Caused by Personnel Error.Station Procedure, Removal & Restoration of Equipment, Not Properly Used. Personnel Instructed by Operating Engineer ML19308A7531978-03-23023 March 1978 RO 269/78-03:on 780222,Unit 2 Field Flashing Breaker Failed to Close.Cause of Breaker Malfunction Not Determined.Relays in Breaker Control Circuit Were Replaced.Investigation to Control Breaker Sys Faults Continues ML19316A4641978-03-15015 March 1978 RO 269/78-04:on 780301,two Reactor Bldg Cooling Units Found Inoperable Simultaneously.Caused by Insufficient Installation Procedures Allowing Trip Point to Be Set Too Low.Breaker Reset & Trip Setpoint Increased ML19316A4171978-02-0303 February 1978 RO 269/78-01:on 780203,field Flashing Breaker Failed to Close.Controls Checked & Found in Proper Condition.Breaker Checked & Cleaned.Cause of Failure Not Determined ML19317F3461978-02-0202 February 1978 RO 270/78-04:on 780202,nuclear Instruments Found Out of Calibr in Less Conservative Direction & Could Have Prevented Fulfillment of Functional Requirements of Reactor Protective Sys.Cause Not Stated.Administrative Measures Taken ML19308A7971978-01-31031 January 1978 RO 269/78-02:on 780105,Keowee Hydro Unit 1 Not Verified Operable within 1-h of Taking Keowee Unit 2 Out of Svc. Caused by Failure to Follow Established Procedures by Personnel.Operators Instructed in Tech Specs ML19317E0451978-01-26026 January 1978 RO 269/77-31:on 771229,leakage of Less than 1 Gallon Per Minute Noted.Caused by Failure of Switch 1PS-364 Diaphragm. Switch 1PS-364 to Be Replaced During Future outage.1PT-21P Switch Recalibr & Returned to Svc ML19316A4841978-01-19019 January 1978 RO 269/77-30:on 771220,primary Leak Through Pressurizer Spray Bypass Valve RC-2 Indicated.Caused by Packing Leak on Pressurizer Spray Bypass Valve.Valve RC-2 Repacked & Tested for Leaks ML19317D9631978-01-18018 January 1978 Incident Investigation Rept RO-B-692:on 780117,Keowee Unit 2 Removed from Svc for Maint & Keowee Unit 1 Not Verified Operable within 1-h Per Tech Specs.Keowee Unit 1 Verified Operable Upon Discovery ML19308A7841978-01-18018 January 1978 RO 269/77-29:on 771219,Keowee Hydro Unit 2 Failed to Start on Initiation from Oconee Control Room.Field Flashing Breaker Failed to Close.Cause Not Determined.Breaker Inspected & Serviced & Found Operable ML19317D9591978-01-13013 January 1978 Incident Investigation Rept RO-B-690:on 780113,indications Reading High During Calibr on a Core Flood Tank (IP/0/A/020/01A).Error May Have Allowed Unit Operation in Violation of Tech Specs 3.3.3 ML19317D8781977-12-19019 December 1977 RO 269/77-28:on 771216,B&W Discovered Min Vol & Concentration Requirements Were Insufficient for Reactor Shutdown.Cause Not Given.Boron Solution Vol Increased to Provide Adequate Margin for Shutdown ML19308B1701977-12-15015 December 1977 RO 269/77-27:on 771215,B&W Discovered Error in Computer Used for Incore Detector Signal Processing.Initial Action to Reduce Positive Imbalance Trip Setpoints by 2.5% ML19317F2651977-12-0606 December 1977 Ro:On 771206,valve 3LP-28 Not Locked Open as Required by Tech Specs.Valve Locked Open Upon Discovery.Forwards Util Incident Investigation Rept B-674 ML19308A8451977-11-10010 November 1977 Ro:On 771107,analysis of Raw Water Supply Samples Collected in July,Aug & Sept 1977 Showed Tritium Concentration Exceeding Control Level by Greater than Ten Times ML19312C6131977-10-31031 October 1977 Ro:On 771026,milk Samples Collected 771005 Showed I-131 Concentrations Exceeded Control Levels Per Tech Specs Section 6.6.2.2.a.Higher Levels Attributed to 770917 Chinese Nuclear Test ML19312C7141977-09-26026 September 1977 Ro:On 770920,radionuclide (Cs-134 & Cs-137) Levels of Keowee River Sediment Samples Collected in Aug 1977 Registered 10 Times Control Level.Based on Diluted Tailrace Concentrations,Levels Lie within Expected Values ML19312C6251977-08-25025 August 1977 Ro:On 770819,fish Samples Collected During July 1977 Showed Cs-137 Levels Exceeding Control Limits by Over Ten Times. Concentrations within Health & Safety Limits & No Corrective Actions Planned ML19312C6181977-08-18018 August 1977 Ro:On 770812,composite Surface Water Samples Collected from Apr-June 1977 Showed Tritium Concentration Exceeding Control Level by 50 Times.No Threat to Public Safety & No Corrective Action Planned ML19317F3221977-08-16016 August 1977 RO 270/77-10:on 770803,reactor Bldg Purge & Penetration Room Ventilation Sys Running Time Check Revealed That Required Surveillance of Filter Sys Was Not Performed.Caused by Failure to Implement Adequate Administrative Procedures ML19317D9971977-08-16016 August 1977 RO 269/77-17A:on 770517,emergency Power Source Inadvertently Isolated.Caused by Procedural Inadequacy of Some Tests. Periodic Test Procedure Revised for Restoring Emergency Power Sys to Proper Lineup 1990-04-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20206P1501999-01-0505 January 1999 LER 98-S03-00:on 981207,security Officer Discovered Uncontrolled Safeguards Info Drawing.Caused by Failure to Follow Established Procedures & Policies.Drawing Was Controlled by Site Security.With ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198E6381998-12-17017 December 1998 LER 98-S02-00:on 981130,security Access Was Revoked Due to Falsification of Criminal Record.Individual Was Escorted from Protected Area & Unescorted Access Was Restricted. with ML20153G4601998-09-30030 September 1998 USI A-46 Seismic Evaluation Rept, Vols 1-2 ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML15261A4681998-09-0404 September 1998 Safety Evaluation Supporting Amends 232,232 & 231 to Licenses DPR-38,DPR-47 & DPR-55,respectively ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20247L9041997-12-31031 December 1997 1997 Annual Rept for Duke Energy Corporation & Saluda River Electric Cooperative,Inc,Financial Statements as of Dec 1997 & 1996 Together W/Auditors Rept ML20198J7651997-10-15015 October 1997 Safety Evaluation Accepting 10-yr Interval Insp Program Plan Alternatives for Listed Plants Units ML20148S3141997-06-30030 June 1997 Ro:On 970422,Oconee Unit 2 Was Shut Down Due to Leak in Rcs. Leak Was Caused by Crack in Pipe to safe-end Weld Connection at RCS Nozzle for HPI Sys A1 Injection Line.Unit 1 Was Shut Down to Inspect Hpis Injection Lines & Implement Ldst Mods ML20148H2501997-06-0505 June 1997 Safety Evaluation Accepting Proposed Restructuring of Util Through Acquisition Of,& Merger W/Panenergy Corp ML20210E3591997-03-27027 March 1997 Part 21 Rept Re Sorrento Electronics Inc Has Determined Operation & Maint Manual May Not Adequately Define Requirements for Performing Periodic Surveillance of SR Applications.Caused by Hardware Failures.Revised RM-23A ML20134N7121997-02-20020 February 1997 Safety Evaluation Accepting Relief Request 96-04 for Plant ML20138L2151997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Oconee Nuclear Station,Units 1,2 & 3 ML20138L2281996-12-31031 December 1996 Revised Monthly Operating Repts for Dec 1996 for Oconee Nuclear Station,Units 1,2 & 3 ML20133C1231996-12-23023 December 1996 Informs Commission of Staff Review of Request for License Amends from DPC to Perform Emergency Power Engineered Safeguards Functional Test on Three Oconee Nuclear Units ML20115F2471996-07-0303 July 1996 Part 21 Rept Re Piping (Small Portion of Unmelted Matl Drawn Lengthwise Into Bar During Drawing Process) Defect That Existed in Bar as Received from Mill.Addl Insp Procedure for Raw Matl Instituted ML20107M8931995-10-31031 October 1995 Nonproprietary DPC Fuel Reconstitution Analysis Methodology ML17353A4341995-10-31031 October 1995 Rev 1 to BAW-2245, Initial Rt of Linde 80 Welds Based on Fracture Toughness in Transition Range. ML17264A1181995-07-31031 July 1995 Response to Part (1) of GL 92-01,Rev 1,Suppl 1. ML20086M0851995-06-29029 June 1995 DPC TR QA Program ML20077R3631994-12-31031 December 1994 Monthly Operating Repts for Dec 1994 for Bfnpp ML20236L5971994-12-29029 December 1994 SER in Response to 940314 TIA 94-012 Requesting NRR Staff to Determine Specific Mod to Keowee Emergency Power Supply Logic Must Be Reviewed by Staff Prior to Implementation of Mod ML20064L2001994-01-31031 January 1994 Final Rept EPRI TR-103591, Burnup Verification Measurements on Spent-Fuel Assemblies at Oconee Nuclear Station ML20062K7481993-12-0101 December 1993 ISI Rept for Unit 2 McGuire 1993 Refueling Outage 8 ML20056E5171993-08-31031 August 1993 Technical Review Rept, Tardy Licensee Actions ML20046C1291993-08-0202 August 1993 LER 93-007-00:on 930701,determined That Unit 1 Ssf Rc Makeup Sys Inoperable in Past Due to Design Deficiency.Operations Procedures Revised to Reflect Newly Calculated Operating Limits for Rc Makeup Pump,Rcps & RCS.W/930802 Ltr ML20056G0131993-07-27027 July 1993 Rev 0 to ISI Rept Unit 2 Oconee 1993 Refueling Outage 13 ML20044G5311993-05-26026 May 1993 Suppl to 921207 Part 21 Rept Re Declutch Sys Anomaly in Certain Types of Valve Actuators Supplied by Limitorque Corp.Limitorque Designed New Declutch Lever Which Will Be Available in First Quarter 1993 ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20117A5981992-11-23023 November 1992 Special Rept:On 921119,ability of Control Battery Racks to Withstand Seismic Event Could Not Be Confirmed & Batteries Declared Inoperable.Batteries Expected to Be Restored in TS Required Time ML20097G0421992-05-31031 May 1992 Analysis of Capsule OCIII-D Duke Power Company Oconee Nuclear Station Unit-3 ML20077D0671991-11-15015 November 1991 Nonproprietary Version of Rev 0 to Boric Acid Corrosion of Oconee Unit 1 Upper Tubesheet ML20067A5241990-12-31031 December 1990 Final Submittal in Response to NRC Bulletin 88-011, 'Pressurizer Surge Line Thermal Stratification.' ML20042F3541990-04-30030 April 1990 Special Rept Re Failure to Prevent Performance Degradation of Reactor Bldg Cooling Units.Caused by Mgt Deficiency & Inadequate Program.Cooling Unit Declared Inoperable & Removed from Svc for Cleaning & Placed Back in Operation ML17348A1621990-03-27027 March 1990 Part 21 Rept Re Matls W/Programmatic Defects Supplied by Dubose Steel,Inc.Customers,Purchase Order,Items & Affected Heat Numbers Listed ML19332D5391989-10-31031 October 1989 Core Thermal-Hydraulic Methodology Using VIPRE-01. ML20042F2321989-08-31031 August 1989 Nonproprietary DCHF-1 Correlation for Predicting Critical Heat Flux in Mixing Vane Grid Fuel Assemblies. ML20205F3211988-10-10010 October 1988 Part 21 Rept Re Potential Deviation from Tech Spec Concerning Ry Indicators Due to Operating Temp Effect on Analog Meter Movement.Initially Reported on 881006.Customers Verbally Notified on 881006-07 ML20154K2091988-09-0909 September 1988 Rev 0 to Response to NRC Bulletin 88-005,Nonconforming Matls Supplied by Piping Supplies,Inc at Folsom,Nj & West Jersey Mfg Co.... Proprietary Procedure 1404.1, Leeb Hardness Testing (Equotip).... Encl.Procedure Withheld ML20245D9541988-09-0606 September 1988 Part 21 Rept Re Condition Involving Inconel 600 Matl Used to Fabricate Steam Generator Tube Plugs & Found to Possess Microstructure Susceptible to Stress Corrosion Cracking ML20245B6061988-08-31031 August 1988 Inadequate NPSH in HPSI Sys in Pwrs, Engineering Evaluation Rept ML20239A6991987-11-30030 November 1987 Addendum 1 to Rev 2 to Integrated Reactor Vessel Matl Surveillance Program (Addendum) ML20236T0791987-11-25025 November 1987 Advises LER 269/87-09,re Degradation of More than One Functional Unit of Emergency Power Switching Logic for Units 2 & 3,in Preparation & Will Be Submitted by 871215. Incident Originally Discussed in Special Rept ML20236Q9491987-10-31031 October 1987 Monthly Operating Repts for Oct 1987 ML20235W9611987-09-30030 September 1987 Monthly Operating Repts for Sept 1987 ML20234B1861987-08-31031 August 1987 Monthly Operating Repts for Aug 1987 ML20237K4761987-07-31031 July 1987 Monthly Operating Repts for Jul 1987 ML20236Y0221987-07-0808 July 1987 Safety Evaluation Clarifying Determination of Acceptability of Test Duration for Performance of Integrated Leak Rate Test at Plant ML20235S6311987-06-30030 June 1987 Monthly Operating Repts for June 1987 1999-01-05
[Table view] |
Text
.,:. 6i Dukeikuwr Compazy - (803) 8a25363
.= 0:ener Nudear Station .
PO Bar H39 '
Seneca, S C 296t9 DUKEPOWER April 30, 1990 i
U. S. Nuclear Regulatory Commission Document Control Desk ;
Washington, DC 20555 E!
Subject:
Oconee Nuclear Station, Unit-3 g Docket No. 50-287 Species 1 Report Concerning Failure to Prevent Performance Degradation of
' Reactor Building Cooling Units o
Gentlemen This report is provided for information regarding failure to prevent performance degradation of. Reactor Building Cooling Units.
If you have any questions, please contact' Rick Matheson at (803) 885-3119..
Very truly yours, MM uw H. B. Barron i Station Manager
/ftr Attachment xc: Mr. S. B. Ebneter Mr. P. H. Skinner Regional Administrator, Region II NRC Resident Inspector i U.S. Nuclear Regulatory Commission Oconee. Nuclear Station 101 Marietta St., NW, Suite 2900 Atlanta, Georgia 30323 INPO Records' Center Suite'1500 Mr. L. A. Weins 1100 Circle'75' Parkway Office o?~ Nuclear Reactor Regulation Atlanta, Georgia 30339 U.S.. Nuclear Regulatory Commission !
Washington, DC 20555 A$
F 9005080221 900430 PDR ADOCK 05000287
.g PDC -
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MANAGEMENT DEFICIENpY RESULTS IN FAILURE TO DETECT PERFORMAM"E i DEGRADATION OF REACTOR BUILDING COOLING UNITS ARSTRACT On February 20, 1990, the Design Engineering Safety Analysis group performed an evaluation of the cooling capacities of the Unit 3 Reactor' Building Cooling Units (9BCUs), based on test data gathered earlier that day. The evaluation' concluded that, assuming a single failure of the'RBCU-train with the highest capacity, service-induced fouling of the two worst' trains, ("A" and "C"), could have prevented-the RBCU system from performingLits intended safety functions.. Immediate corrective action was taken at 1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br />, as soon as the evaluation results were received at the station; RBCU train "C" was declared inoperable, placing the unit into a seven day ILO; the 3B train was placed in operation; and then the 3C RBCU was taken out of service for cleaning and testing. At 1334 hours0.0154 days <br />0.371 hours <br />0.00221 weeks <br />5.07587e-4 months <br />, on=
February 122, the 3C RBCU was declared operable following testing which indicated capacity was 61% of design capacity. Subsequent corrective actions vore to clean and test the "A" and "B" RBCU trains. Previous LERs have reported Oconce, Nuclear Station's recurring problems with RBCU
' degradation. Corrective actions from the earlier LERs were not adequately implemented therefore the Root Cause of this event is attributed to Management DefJclency, inadequate program. This event is being reported as a Special Report. ,
BACKGROUND The Reactor Building Cooling System [ Ells:BKl is an Engineered Safeguards (ES) System [ Ells:JE) which, in conjunction with other ES systems, provides heat removal capability for the containment atmosphere during normal and post-accident conditions. The system consists of three Reactor BuildinR Coolant Unit (RBCU) trains that function as' air-to-water heat l
exchangers, located entirely within the Reactor Building (RB) [EIIS:NG).
During. normal operation, trains "A" and "C" operate with fans in high speed while the "B" train f an is of f. Iow Pressure Service Water (LPSW)
[E!IS:BI] flow is also diverted from the "B"-RBCU to the non-safety j related Reactor Building Auxiliary Cooling (RBAC) [EIIS:BK) units, r ollowing an accident, such as a LOCA, an ES signal automatically aligns LPSW to the "B" RBCU and fans on all three RBCU trains'shif t to low speed.
The fans force containment air across RBCU cooling coils and reject RB
!. energy to the environment via the LPSV system. Following an accident, the l RBCUs help to ensure that post-IDCA conditions do not exceed the l
environmental qualifications (EQ) of RB equipment required to be operable to mitigate the consequences of a' LOCA. The station Final Safety Analysis Report Section 15.14.5 states that RB design pressures will not be exceeded following a worst-case LOCA even without any RBCU capacity. RBCU
.l operability criteria is therefore based solely upon the ability to maintain the RB environment within the EQ envelope following a LOCA and assuming a single failure of the RBCU train with the highest capacity.
I
n . .g. , %[ _
i Technical Specification 3.3.5 requires ti.at the station enter a seven day.
Limiting Condition of Operation (LCO) if less than 3 operable RBCU trains are available during power operations. While the station is in an LCO due to an inoperable RBCU train there is no requirement to consider a-single-f ailure of the worst train when determining operability of the RBC -
system.
EVENTS DESCRIPTION i
Service induced fouling of the Reactor Building Cooling Units (RBCUs) heat transfer surfaces has been identified as a~ problem at Oconee Nuclear "
Station since 1986, particularly in Unit 3. LERs 269/87-04, 287/88-03, and 287/89-01 reported events where cooler degradation caused the unit to be shutdown or resulted in the establishment of power level limitations.
The corrective cetions specified in these LERs, in part, required an increased frequency of performance testing. to ensure that fouling of the
- coolers was trended and the coolers cleaned prior to.the point where i degradation caused the RBCUs to be inoperable.
Several factors hindered station personnni 'in .their. attempts to anticipate the extent of cooler fouling and ensure that cleaning of the cooler coils was performed before degradation caused the coolers to be inoperable.
- 1) The rate of degradation is af fected by numerous variables- RB and LPSW temperatures, building humidity, boron concentration in the Reactor Coolant System (RCS) [EIIS:AE], and RCS' leakage rate, to name a'few. Unit 3's degradation rate is particularly difficult to characterize.
- 2) It is generally accepted that baron from RCS leaks is the main-
' contributor to the particulate which-is causing cooler surfaces to foul, however, the octual transport mechanism is not completely understood and therefore t he actions necessary to ,
prevent or limit the rate of fouling are not readily determined. !
Specific corrective actions required by previous LERs are as follows:
LER 287/88-03 Perform test.ing of Unit 3 RBCUs " periodically with frequency '
adjusted as necessary."
LER 287/89-01
- 1) Establish a task force to determine the cause of, and provide recommendations to prevent, cooler fouling.
- 2) Install experimental instrumentation to allow continuous monitoring of Unit 3 RBCU status during unit operations.
- 3) Do performance tests of Unit 3 RBCUs "as required based on-l indication of the installed experimental instrumentation
- l. and results of safety analysis performed af ter testing."
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. q Also, In order to establish a broader base for cooler performance, the :
RBCU task force decided to perform tests prior to shutdown for refueling as well as following Unit. start-up. The' data obtained from all performance testing is transmitted to the Design Engineering-(DE)
-Mechanical Oconce Systems Engineering (MOSE) group.
MOSE personnel use the data provided to calculate the heat removal i capacity of each RBCU train as well as- ;.he rate of degradation given the current lake water temperature. This information is provided to the DE Safety Analysis (DESA) group.
DESA prepares an Operability Evaluation (OE), also referred to as a safety ,
analysis in previous LERs, which is, in part, an estimate of how long the coolers will remain operable based on the current capacity and calculated degradation rate. The OE is sent to the station Compliance section for review and distribution at the station. Performance Engineer."A" (PE "A")~
and MOSE DE "A" (DE "A") agreed that the RBCUs were to be tested approximately half-way through the operable period established by DESA.
This was believed to be a suitably conservative testing frequency.
A task force was established in January,1989 with PE "A" acting as the c.hnirman. The group was comprised of members from various station organizations and DE. Between January and mid-1989 the task force met regularly and made significant contributions to the RBCU problem resolution effort.
}
The task force developed an effective cooler cleaning method and deduced 'l that the source of the fouling was baron, likely from RCS leakage, i precipitating out on cold cooler tubes. In addition, the task force was 1 able to determine that- tube side fouling was not a significant source of cooler performance degradation. Af ter June of 1989, however, the full task force no longer functioned as a viable organization; meetings were ]
inf requent and not well attended, and there was no consistency cf support !
from the most station sections ~. A core group comprised of_ members from l the Performance, Operations, Maintennnce Engineering, and' Design _ l
- . Engineering Sections still continued to work together to resolve critical l L issues. 1 i
In late February 1989, experimental Instruments (hygrometers) were in=talled in accordance with LER 287/89-01 and Temporary Modification 515 l to allow cont (nuous monitoring of RBCU performance. Results were ;
encouraging and it nppeared that the use of the new instruments would 3 enhance the performance testing program but thn experimental Instruments ;
failed due to the harsh service environment within approximately 8 weeks of installation. Attempts to find suitable replacement instruments l capable of withstanding the environment continued until November 1989, at l which time replacements were ordered.
On November 2 1989, prior to shutting down for refueling outage (RFO) 11 l on Unit 3, PE "A" coordinated the testing of the RBCUs. The test results
]
indicated that the coolers were quito clean, as evidenced by the heat j trans fer capacity available. (Subsequent visual inspection, performed !
while RF0 11 cleaning of RBCUs took place, verified cooler cleanliness). Y DESA provided an Operability Evaluation (OE) to the station based on the l
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[
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test data. This evaluation. indicated that_the RBCUs would remain operable until November, 1990.
Although the performance tests indicated that the coolers were clean, Operations personnel entered the Reactor Building as part of a normal pre-shutdown tour, and attempted to identify potential sources of airborne boron. No now sources of RCS leakagn were identified. !
During the Unit.3 RF0 the coolers were all cleaned using hot water. This-wns the cleaning method which had proven to provide the best results.
Unit 3 was started up on December 20, 1989 and, after allowing some time. l for RB and system temperature stabilization, on January.9, _1990, a ;
performance test of Unit 3 RBCUs was performed.' The results of this test j indicated that there had been substantial fouling of all three RBCUs in j the relatively brief (approximately 20 days) period since unit startup, j l
PERCENT OF DESIGN CAPACITY- l (100 % = 80.tfillion BTU /Ur) l 1
TEST DATE "A" RBCU "B" RBCU "C" RBCU i i
11/2/89 98% 104% 92%
01/9/90 55% 71% 55 (64%) l PE "A" and DE "A" discussed the test results and determined that .!
conditions at the time of the test were sufficiently different from !
conditions when the November 7 test was performed to have skewed the 'j results: The January test was performed with a relatively cool-and dry RB n which caused a much lower RB-to-LPSW delta temperature-(d/t). This lower d/t was believed to have the not effect of making the coolers appear to be ,!
less officient than they actually were. Another factor which caused the j test results to be questioned was the 33% degradation of the "B" cooler in l spite of the fact that it had not. been operated since it was last cicaned. ,
Current thinking presupposed that degradation occurred as a result of [ '
baron in the RB atmosphere plating out on the cold surfaces of an in-service cooler. A degraded "B" cooler implied to PE "A" and DE "A" {
that the test results were not representative of the actual status of the {
coolers. A second test performed later on January 9th, at slightly higher j RB temperat.ures, indicated a 64% capacity for the 3C RBCU. This 9% !'
increase over the earlier test suggested that cooler performance was more sensitive to building heat load (and d/t) than was originally thought. {
PE "A" discussed the testing results and conclusions drawn with j Performance Supervisor "A" (PSA) and the Performance Manager (PM). j i
Although the OE provided to the station on November 7 indicated that Unit !
3 RBCUs would be operable until November, 1990, and PE "A" and DE "A" both .;
believed that the January 9 test results were not representative of the !
actual cooling capacities, it was decided to perform another set of RBCU tests in the near future to confirm that higher RB temperatures would ;
result in more accurat.e test results. It was the consensus opinion that if the next test could be done at conditions closely approximating the November test the results would also mimic the earlier test results.
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. .5-It should-be noted that Operations (OPS) personnel were aware that a test of the RBCUs was performed in January. OPS is normally made aware of the test results'when the OE is distributed to them after being reviewed by the station Regulatory Compliance group. However, since the OE statement performed in November, 1989 indicated the coolers were expected to be operable until the following November, DE "A" and PE "A" determined that a new OE need not be performed. OPS management was not informed of the. test results and therefore had no inkling that the test indicated that degradation appeared to have occurred at a greater than expected rate. It.
should be noted that even if the degradation had occurred to the extent Indicated by the performance tests,-the coolers were still operable at this time.
On February 2, 1990, PE "A". noticed an increasing trend in RB temperatures and discussed this trend with the Unit 3 Operations Coordinator on ,
February 14, 1990. On February 16, Unit 3 Operations Manager (OM) roccived the Unit 3, EOC-11 RBCU Haintenance Technical Report from the station Maintenance Engineering Services group. This report included a
" Findings /Results" section which' stated, la reference to the January 9 r test results, that though the numbers did not indicate it, the cleaning of the-coolers during the RF0 "most likely increased the heat removal-capability of the coolers."
On February 17, 1990, Shift Supervisor "A"-(SS "A") was informed by a Senior Reactor ~0perator (SRO) that the 115 degree F. RB temperature limit-of PT/3/A/600/0, " Periodic Instrument Surveillance" had been reached and notification of OPS management was required. On Honday, the 19th,'SSA.
discussed the rising RB temperature with OM, expressed his' concerns that the coolers were fouled, and made plans to do a building entry the next day. That afternoon discussions between OPS and Performance personnel resulted in the decision being made to perform on RBCU performance test as soon as practical. A plot of RB temperatures continued to show.an increasing trend which caused unanimous concern.
On Tuesday morning, February 20, 1990, SSA and an OPS Nuclear Production Engineer (NPE) entered the RB to attempt to identify potential sources of I
RCS leaks and'to make a visual inspection of the Reactor Building Auxiliary Coolers (RBACs). No new sources were found but the inspection l
did reveal a significant amount of fouling on the RBAC coils-indicated by the almost complete lack of any air flow across the coils. Fouled RBAC coils can be on indicato of RBCU coil condition.
l On Tuesday afternoon, the 3A and 3C RBCUs were tested and-the results were verbally communicated to DE. DE "A" analyzes the test. data to determine cooling capacities. The analysis indicated that the coolers had' degraded i and had unacceptable capacities:
3A RBCU - 25.0% of Design 3C RBCU - 23.0% of Design i At 48% combined capacity, and assuming a single failure of the "B" train, cooling capacity was insufficient to allow operation at 100% reactor power. DESA determined that a minimum of 82% capacity was required from the two worst coolers to allow operation at 100% reactor power. It could not be determined when cooler degradation had progressed to the point
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where available capacity was insufficient to allow operation at 100%
power.
t Consequently, after discussion between OPS, Performance, and Compliance personnel, the decision was made to declare the 3C RBCU inoperable and '
take it.out of service for cleaning .and testing. Therefore, at 1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br />, on February 20, 1990, wit.h Unit 3 at 100 % Full Power, the "C" '
train was declared inoperable which caused Unit 3 to enter a seven day Limiting Condition of Operation (LCO) in accordance with Technical Specification 3.3.5. The "B" RBCU train was , aced in operation while cleaning and testing of the "C" train was pe:( aned. Although the "B" train capacity was not tested prior to placing it in service, it was ;
assumed to be 71% based on the January 9th test results and the. fact thac the "B" train had not bann operated since that date. The 3B RBCU was tested later on the 20th and had an indicated capacity of 68L ,
While the station was in the LC0 there was no -' longer the requirement to assume a single failure of the best train. Instead, operation at 100%
power was dependent upon the combined capacities of the two operable trains, in this. instance, "A" and'"B". The combined cooling capacity was 25% + 68% = 93%, more than the 82% required to allow operation at 100%
reactor power. The "C" cooler was' cleaned and performance tests indicated a 61% cooling capacity and, therefore, _at 1334 hours0.0154 days <br />0.371 hours <br />0.00221 weeks <br />5.07587e-4 months <br />, on February 22, 1990, the 3C RBCU was declared operable and returned to service. Once the 3C train was cleaned and back in service the event was terminated since a combination of any two RBCU trains then had the necessary post-accident cooling capacity. Subsequent actions taken were to clean and test the "A" and "B" RBCU trains.
CONCLUSIONS The Root Cause of this event is determined to be flanagement Deficiency, inadequate program due to failure to adequately implement previously specified corrective actions. Rather than establishing formal and detailed guidelines for the accomplishment of corrective actions in order to assure that Reactor Building Cooling Units were maintained operable, the program was allowed to evolve ~ over time as testing provided new -
information. While such latitude was conducive to allowing the program to be enhanced and refined, it included limited controls or balances for
- those responsible for implementation of the testing program. Given Unit ,
3's past problems and historically erratic fouling rate it is concluded that the program should have provided more guidance and should have been more closely scrutinized by management.
l' The Root Cause identified in previous LERs was Other, due to service induced fouling. The root cause of this event is flanagement Deficiency due to failure to prevent recurrence of a previously identified recurring problem. Because the problem was not corrected this event is considered to be recurring in spite of the fact that the root cause determinations are different. Corrective actions from previous reports have already been addressed in this report.
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,s There were no radioactive _ material releases,. radiation exposures, or personnel injuries as a result of this~ event. The event did not involve equipment failure and'is not.NPRDS reportable.
CQRRECTIVE ACTIONS i IMMEDIATE
- 1) . The 3C Reactor Building Cooling Unit (RBCU) was declared _
inoperable, removed from service for cleaning, and placed back j
i in operation following evaluation to ensure effectiveness of the cleaning.
2)- The "B" RBCU train was placed in service.
' SUBSEQUENT
- 1) The 3A and 3B RBCUs were cleaned and tested.
PhANNED '
- 1) The RBCU Honitoring Program will be formalized as a section in the Performance Manual to define the monitoring process. 'l
- 2) The Performance Section will revise the procedure used,to gather data for RBCU operability evaluations. Tho' procedure will be j used as the mechanism to control the Monitoring Program and will l include:
i
-n. The method for gathering data,
- b. Controls for transmittal of test _ data to Design Engineering (DE). :
I
- c. Controls to ensure appropriate station personnel are notified of RBCU operability status. ;
- d. Limits and actions to be taken based on operability margin.
- 3) The RBCU Task Force will be reactivated to pursue a solution to fouling problems and seek methods to ' locate sources of the-fouling. The Task Force will disband af ter completing its 3 mission and will notify Station management, in writing, of its -1
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Intent to disband. The Task Fa ce will oversee the following '
activities;
- a. The Nuclear Performance Evaluation section will investigate !
the feasibility of'an on-line spray system to prevent fouling of the air side of the cooling coils.
- b. DE will investigate the feasibility of performing an i evaluation to show that the amount of service induced fouling which typically occurs during 1 refueling cycle would not' prevent the RBCUs from performing their intended safety function. ,
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.c.. The Task Force will investigate reducing the opportunity I for fouling by limiting low Pressure Service Water flow :
through the RBCUs.
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- d. The Maintenance group wil1 develop and lui ready to implement a plan to search for Reactor Coolant System leakage during unit trips and outages.
SAFETY ANALYSIS 1 f
Degraded Reactor Building Cooling Unit-(RBCU) capacity has little impact, on' peak Reactor Building (RB) temperatures' following the most severe-Design Basis (DB) accident but will slightly increase the cooldown time.
- The concern is that, immediately-following a DB LOCA, inadequate RBCU capacity might result;in environmental conditions which could adversely: ,
impact the ability of important safety systems to perform their intended function. The' operability criterion that the RB temperature profile remain within the environmental' envelope for a DB TOCA assures that safety systems remain operable. For operability determination purposes it is implicit that maintaining RB temperature.bolow the Environmental' Qualification (EQ) envelope will also ensure that design RB pressures.will ,
not be exceeded.
The Design Engineering and Performance personnel involved in performance testing and trending of cooler degradation rates have speculated that the capacities of the RBCUs would actually be much improved during a DB accident regardless.of their relative cicanliness prior to the start of the accident. This reasonirg is logically supported although as yet it.
has not been empirically proven.
The support stems f rom thn similarity between the cooler coll . cleaning, method used by the-station and RB' conditions following an. accident. The method of cooler cleaning employed by station Maintenance Support. . .
personnel is to pour approximately 200-300 gallons of hot.(almost boiling)
- water over the coils .and let the water gravity drain to the RB basement.
L Experience has shown that the hot water dissolves the encrusted boron deposits and transports the soluble boron to.the building sump. .The -
effectiveness of this cleaning method has been proven by both visual examination and post-cleaning performance testing.
l E
It is believed that the RB environment will similarly act to clean the l' coolers following a DB LOCA. Design conditions following an accident result in a steam-air mixture at 286 degrees Fahrenheit (deg. F.), a RB pressure of 73 psia, a Inkn water inlet temperature of 75 dog. F., and a worst case baron concentration at start of core life.
L At 286 degrees, water is calculated to be able to hold (or dissolve) 95,883 ppm baron (which is greater than. worst case concentration by nearly a factor of 100) and it is estimated that,'following a DB LOCA, each RBCU
- l train will be condensing close to 130 gpm of RB steam-water mixture. This .
I volume of hot water pouring over the cooler tube surfaces will be
a cleaning method even more effective than the one which is currently used -
and has proven so effective. The engineering judgement of several Duke organizations supports the premise that a self-cleaning phenomena will occur _following an accident and the coolers will be able to provide the cooling necessary to ensure post-accident EQ limits are not violated, None the less, as has been stated, our current accident scenarios require
-adequate RBCU capacity be available in the event of a LOCA and,_ for some indeterminate period of time preceding February 20, 1990', the Unit 3A and 3C RBCUe had inadequate cooling capacity available. .llowever, no accidents requiring the mitigating function of the RBCUs occurred and there were no '
radiological releases associated with this event, therefore the health and safety of the public was not affected. -
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