ML17340A157

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LER 80-015/03L-0:on 800802,during Power Operation & in Preparation to Increase Vol in Accumulators,Safety Injection Pump 3A Failed to Start Following Manual Initiation.Caused by Broken Support for Driving Pawl
ML17340A157
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 09/02/1980
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17340A156 List:
References
LER-80-015-03L-01, LER-80-15-3L-1, NUDOCS 8009120385
Download: ML17340A157 (4)


Text

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following manual initiation. The problem was traced to the 3A SI pump's 5

4160V breake . A spare breaker was installed, in the breaker cubicle, tested, and the 3A SI'pump declared operable within 40 minutes. During this event, the 33, 4A, a 4B SI pumps were operable and available. An 1

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evaluation to determine reportability pursuant to I.CAIRO

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~i o The cause of the inonerabilitv was a bxoken su ort for the drivin awl xesulting in inability to charge the closing spring. An evaluation is in progress to detexmine the cause of the broken support. Our daily inspection oz safety related 4160V spring position and annual physical inspect'on will continue while the evaluation is in progress.

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REPORTABLE OCCURRENCE 250-80-15 LXCENSEE EVENT REPORT PAGE TWO Component Data:

I GE Magne-Blast Circuit Breaker Type AM-4.16-350-1H