ML17339A403

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LER 79-034/03L-0:on 791105,during Power Operation,Auxiliary Feedwater Pumps Tested & Pump a Failed to Start.Caused by Misalignment Between Connections to Associated Pneumatic Controller Resulting in Inoperability of Valve CV-3705
ML17339A403
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 12/05/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17339A402 List:
References
LER-79-034-03L, LER-79-34-3L, NUDOCS 7912190522
Download: ML17339A403 (3)


Text

NAC POAIII 366 ,P~21 LICENSEE EVENT REPORT U.*o4UCLEAA REGULATORY COY!VIISSICI 1 I ll 1 I 1 Q~I Oe LoCfleSK TVPK JJ 5~Ae Sa 0 C.4 2$28 I I Ol (PLEASE PRINT OR TYPE AI.L REQUIAcO INPOAAIATIONI I~QI l LI OPf St3 C2 I I-0 lO~Ot 0!0-lO 1 3 9 LICKASKK COOK LICK 43%e'<<>Sea CON'T e'O~!>>'O~it O 3 SO Sl QOCKcTPIVNScil 33 33 KV foci QATK IS AKPQAT QATK 3O EVENT OESCRIPTION

'NO PRCEAELE CQ.ISEQUEVCES OIQ~02 Durin o ation, the AHT, s were bein tested in accordance

~os with TS 4.10.1.The"A" AFh faz1ed to start.The B and C"A" AHp pung was-tested and returned to service within 29 minutes.This 9 is the first failure of this ion have been reported ho%<ever, this%%as the f irst occurrence attributed to the cause described belofa in the Cause Description.

~oa 1 S 9 34~Og valve CV-3705.The root cause o~this ino abilitv was a misali~mt svs~KU CAUS%CAUS%CQs!P, yAe yc COOK COOK SU%COOK CCSIPCVKNT COOK SUSCQOK SU%COOK~S LJIQ LJQ~~S LJS LJO 1 3 9 III II 10 Is IS Ig%)ScQUC.VTIAI

.OCCUQAKVCK Af PQIIT II%VISION Lcp,QQ\VCNT Vf Ail 1IKPQIITleo Qi Ty ps 40.0>>'"'o"~1>~~04~~~O!3~L 21 2'I 2 24 33 21 SI 32 4 T!04 F CIJPK KPCCC.Srre'TQQWIV AT,ACIellfooT PePIIQ~PVIIcc r QeJP CQAIPCPI%4T TAKKN Ase!QNo PLANT SIKTrooo IIQ'JPS 22 SUSNI.TKQ FCASISUS.SUPc'ecA YAVUFACTUilcrl L-" I-"'0 LJQ LJQ~Les cJS LJo 35 35 40 41 42 43'1 CAUS O SCRIPToON<<NO CQRREC IVE ACTIOPes O2r o The failu e of the"A" AHJ.to sta<resulted frcpz inooerabili of between the connections to the associated neivetic controller.

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LICiBlSEE EVENT REPOBT PAGE Dv'0 Additional Cause Descri on and Corrective Actions: 1 The failure of the."A" AHJ pump to start resulted fran inoperability of CV-3705 ("A" AEN steam turbine pressure control valve).We root cause of this inoperability was a misalignment between the manifold plugs of the pneumat.c controU.er manifold assenbly and its naunting base assembly due to loose mounting screws.The misalignment was a randan event.Existing preventive maintenance and AHV system periodic testing will provide assurance that a reoccurrence of this type of event will be promptly detected.nent Data: Bailey I~wter Co.Pneumatic Controller

~AD