05000250/LER-1979-034-03, /03L-0:on 791105,during Power Operation,Auxiliary Feedwater Pumps Tested & Pump a Failed to Start.Caused by Misalignment Between Connections to Associated Pneumatic Controller Resulting in Inoperability of Valve CV-3705

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/03L-0:on 791105,during Power Operation,Auxiliary Feedwater Pumps Tested & Pump a Failed to Start.Caused by Misalignment Between Connections to Associated Pneumatic Controller Resulting in Inoperability of Valve CV-3705
ML17339A403
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 12/05/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17339A402 List:
References
LER-79-034-03L, LER-79-34-3L, NUDOCS 7912190522
Download: ML17339A403 (3)


LER-1979-034, /03L-0:on 791105,during Power Operation,Auxiliary Feedwater Pumps Tested & Pump a Failed to Start.Caused by Misalignment Between Connections to Associated Pneumatic Controller Resulting in Inoperability of Valve CV-3705
Event date:
Report date:
2501979034R03 - NRC Website

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LICiBlSEE EVENT REPOBT PAGE Dv'0 Additional Cause Descri on and Corrective Actions:

1 The failure of the."A" AHJ pump to start resulted fran inoperability of CV-3705 ("A" AEN steam turbine pressure control valve).

We root cause of this inoperability was a misalignment between the manifold plugs of the pneumat.c controU.er manifold assenbly and its naunting base assembly due to loose mounting screws.

The misalignment was a randan event.

Existing preventive maintenance and AHV system periodic testing will provide assurance that a reoccurrence of this type of event willbe promptly detected.

nent Data:

Bailey I~wter Co.

Pneumatic Controller

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