ML17338A693

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LER 79-006/03L-0 on 790322:packing leak-off Observed on Three Valves.Cause Undetermined for Two Valves.Leaking Packing on Third Due to Broken Bellows Seal.Unit in Reeling Shutdown;Repairs Will Be Made Before Return to Power
ML17338A693
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 04/20/1979
From: SCHOPPMAN M A
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17338A692 List:
References
LER-79-006-03L-02, LER-79-6-3L-2, NUDOCS 7905080571
Download: ML17338A693 (4)


Text

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QIO Due to RCS.leakage of 2.S5 gpm, the uni.t was shutdown to permit entry inside the containment.

biological shield-Investigation showed valve 1 packing leak-off to the.RCDT from pressurizer valves.'tlinor leakage from a swagelok,fitting at.the incore detector seal table was also observed.I Following evaluation by'he Plant Nuclear Safety Committee, the unit was~returned.to power and the leak rate was checked each shift to monitor 0 S trends in water invento sYs i zM'AUsa CAUss C yp IAl.yr.cadi coos suscaaa 20..>>a¹NTcaos suacaos suscoas LJHoz LJso LJos~i"'zs L'Jzs Lzzs g 10 It 12 12 13 lg 20 Scau SN TI*I, OCs,itzRF IJC RSPOIET 21 22 2$23 ig A=TION puTURs=FFacr szsuroaNN i.scwucNT AINROA PRIucc yr.TAS'4 ACTION ON PLANT AI=TIIaa ROURS Q 4"gsll~=0 Foot;I Nua.Sl Pis,-q ixlSLJos LJsz LJos LLJ>>'IRO 2Joz I*zs 24 SS So 40 4 I 42 42 CAUSc OHCRIPTION ANO CORA-""CTIVS RCTIOz4S O22 R KVISIOAI~6'aulsaNczslr 30 41 The cause of the ackin leak-off could not be determined on two o f'he valves.The leaking packing on the third.vajve was due to a broken bellows seal.The unit is currently in refueling shutdown and repairs I 2 will be completed prior to returning to power.a g FACIUTY STATUS A Pavlalt OSO s~EQzs~OI 9[3 Q NA 2 a 10 12 44 ACTIVITY CONTassr RSLSASSO OF Rcl.SASc AMOU SIT OF*CTIsll TY Q~+Pgg~zgs~zgI NA I 3 9 10 I I 44 PSRSazAVSI.

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~ZQ2 2'0 Puauclry ssuio asscp>>ttaN Q fN~QI 10 NA NAvs o p PRcpRcR N.A.Scho man 79050805 t t.iacRC US-Qssl y sa 30 (305)552 3802 Cg 0 REPORTABLE OCCURRENCE 251-79-6, LICENSEE EVENT REPORT P E AG TWO Additional Event Descri tion and Probable Conse uences The Plant Nucleary Safety Committee (PNSC)'reviewed the evaluation of the Unit 4 Reactor Coolant System leakage rate that was in excess of 1 gpm.The sequence of events and the evaluation follows: By 3:00 PH, March 20, 1979, it was tentatively determined that the source of the excess leakage was from: (1)Xhe 4A Reactor Coolant Pump number'seal leak-off as there were periodic, standpipe"high.level" alarms, (2)'valve packing leak-off to the Reactor Coolant Drain Tank (RCDT)as~observed by periodically needing to quench the Reactor Coolant Drain Tank to maintain temperature below 180'F,.and (3)the 4A and 4B charging pump seal pots overflowing.

The leak rate remained stable at approximately 1.60 gpm through 7iednesday, March 21,'1979.By about 7:00 AH on Thursday,.Harch 22, 1979, the leak rate had increased to 1.85 gpm and by 12:30 PH had increased to 2.85 gpm.At about 1 35 PH, the decision was made to place the reactor in hot shutdown in order to make entry inside the containment biological shield to determine the source of the increased leak rate.The reactor was in hot shutdown at about 2:40 PH.At 4:45 PH, a containment entry was made.The source of the leaks was found to be valve packing leak-offs to the RCDT from pressurizer valves HOV-4-535, HOV-4-536 and PCV-4-455A.

In addition,.

a minor leak was found from a swagelok fitting at the incore detector seal table for one of the score detector thimbXes that was draining to the containment sump.'ll leaks were evaluated as minor.At about 8:30 AH on Friday, Harch 23, 1979, a second containment entry was made to ensure that all leakage areas had been identified and that the leakage at the incore detector seal table had not increased.

No additional leaks were found and the leak rate at the incore detector seal table had not increased above the orig-inal leak rate observed.Unit 4 was returned to service at about 2:40 PH on Friday, March 23, 1979.The PNSC agreed with the evaluation that the leakage rate was minor.and recommended

the leak rate be checked once per each 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shift in order to monitor trends in the water inventory.

The PNSC determined operation of Unit 4 with this leakage would not involve any unreviewed safety questions.

At about 7:00 AH on Tuesday, March 20, 1979, the routine calculation of RCS leak rate indicated a leak rate of 1.27 gpm.-.An investigation was initiated to determine the source of this, excess leakage.

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