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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352  
{{#Wiki_filter:UNITED STATES
    January 31, 2011  
                            NUCLEAR REGULATORY COMMISSION
  Mr. Michael J. Pacilio Senior Vice President, Exelon Generation Company, LLC  
                                              REGION III
President and Chief Nuclear Officer (CNO), Exelon Nuclear  
                                2443 WARRENVILLE ROAD, SUITE 210
                                        LISLE, IL 60532-4352
                                          January 31, 2011
Mr. Michael J. Pacilio
Senior Vice President, Exelon Generation Company, LLC
President and Chief Nuclear Officer (CNO), Exelon Nuclear
4300 Winfield Road
Warrenville IL 60555
SUBJECT:        BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION
                REPORT 05000454/2010-005; 05000455/2010-005; 07200068/2010003-2
Dear Mr. Pacilio:
This refers to the inspection completed on December 31, 2010 at your Byron Station, Units 1
and 2. The enclosed report presents the results of this inspection which were discussed on
January 14, 2011, with Mr. B. Adams, and other members of your staff.
During this inspection, the NRC staff examined activities conducted under your license as they
relate to public health and safety to confirm compliance with the Commission's rules and
regulations and with the conditions of your license. Within these areas, the inspection consisted
of selected examination of procedures and representative records, observations of activities,
and interviews with personnel.
Based on the results of this inspection, the NRC has determined that two Severity Level IV
violations of NRC requirements occurred. The NRC has also identified one issue that was
evaluated under the risk significance determination process as having very low safety
significance (Green). The NRC has determined that one violation is associated with the
issue. These violations are being treated as Non-Cited Violations (NCVs), consistent with
Section 2.3.2 of the Enforcement Policy. These NCVs are described in the subject inspection
report.
If you contest the subject or severity of these NCVs, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
Office at the Byron Station. In addition, if you disagree with the cross-cutting aspect assigned to
any finding in this report, you should provide a response within 30 days of the date of this
inspection report, with the basis for your disagreement, to the Regional Administrator,
Region III, and the NRC Resident Inspector at the Byron Station.


4300 Winfield Road
M. Pacilio                                  -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website
at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                            Sincerely,
                                            /RA/
                                            Eric R. Duncan, Chief
                                            Branch 3
                                            Division of Reactor Projects
Docket Nos. 50-454; 50-455; 72-068
License Nos. NPF-37; NPF-66
Enclosure:    Inspection Report 05000454/2010005; 05000455/2010005; 07200068/2010003
                w/Attachment: Supplemental Information
cc w/encl:    Distribution via ListServ


Warrenville IL  60555
          U.S. NUCLEAR REGULATORY COMMISSION
SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT 05000454/2010-005; 05000455/2010-005; 07200068/2010003-2 Dear Mr. Pacilio: This refers to the inspection completed on December 31, 2010 at your Byron Station, Units 1 and 2.  The enclosed report presents the results of this inspection which were discussed on January 14, 2011, with Mr. B. Adams, and other members of your staff. During this inspection, the NRC staff examined ac
                          REGION III
tivities conducted under your license as they relate to public health and safety to confirm compliance with the Commission's rules and
Docket Nos:         05000454; 05000455; 07200068
regulations and with the conditions of your license.  Within these areas, the inspection consisted
License Nos:       NPF-37; NPF-66
of selected examination of procedures and representative records, observations of activities, and interviews with personnel.
Report No:         05000454/2010005; 05000455/2010005;
                    07200068/2010003
Based on the results of this inspection, the NRC has determined that two Severity Level IV
Licensee:           Exelon Generation Company, LLC
violations of NRC requirements occurred.  The NRC has also identified one issue that was
Facility:           Byron Station, Units 1 and 2
evaluated under the risk significance determination process as having very low safety significance (Green).  The NRC has determined t
Location:           Byron, IL
hat one violation is associated with the issue.  These violations are being treated as Non-Cited Violations (NCVs), consistent with Section 2.3.2 of the Enforcement Policy.  These NCVs are described in the subject inspection
Dates:             October 1, 2010, through December 31, 2010
report.  If you contest the subject or severity of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Inspectors:         B. Bartlett, Senior Resident Inspector
Regulatory Commission, ATTN:  Document Control Desk, Washington, DC 20555-0001, with a
                    J. Robbins, Resident Inspector
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
                    M. Bielby, Senior Operations Engineer
Office at the Byron Station.  In addition, if you disagree with the cross-cutting aspect assigned to
                    R. Edwards, Reactor Engineer
any finding in this report, you should provide a response within 30 days of the date of this
                    M. Learn, Reactor Engineer
inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Byron Station. 
                    B. Palagi, Senior Operations Engineer
  M. Pacilio    -2-
                    L. Rodriguez, Reactor Engineer
                    C. Tilton, Senior Reactor Engineer
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the
                    M. Jones, Reactor Engineer
NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's document system (ADAMS). 
                    C. Thompson, Resident Inspector,
ADAMS is accessible from the NRC Website
                    Illinois Department of Emergency Management
at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). 
Approved by:        E. Duncan, Chief
Sincerely,  /RA/  Eric R. Duncan, Chief
                    Branch 3
Branch 3
                    Division of Reactor Projects
Division of Reactor Projects
                                                                Enclosure
  Docket Nos. 50-454; 50-455; 72-068
License Nos. NPF-37; NPF-66
Enclosure: Inspection Report 05000454/2010005; 05000455/2010005; 07200068/2010003  w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ 
Enclosure
U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos: 05000454; 05000455; 07200068 License Nos: NPF-37; NPF-66 Report No: 05000454/2010005; 05000455/2010005;   07200068/2010003 Licensee: Exelon Generation Company, LLC Facility: Byron Station, Units 1 and 2 Location: Byron, IL Dates: October 1, 2010, through December 31, 2010  
Inspectors: B. Bartlett, Senior Resident Inspector J. Robbins, Resident Inspector  
M. Bielby, Senior Operations Engineer  
R. Edwards, Reactor Engineer  
M. Learn, Reactor Engineer  
B. Palagi, Senior Operations Engineer L. Rodriguez, Reactor Engineer  
C. Tilton, Senior Reactor Engineer  


M. Jones, Reactor Engineer
                                        TABLE OF CONTENTS
C. Thompson, Resident Inspector, 
SUMMARY OF FINDINGS ........................................................................................................... 1
  Illinois Department of Emergency Management
REPORT DETAILS ....................................................................................................................... 3
Approved by: E. Duncan, Chief
Summary of Plant Status ........................................................................................................... 3
Branch 3
  1.   REACTOR SAFETY ....................................................................................................... 3
Division of Reactor Projects 
      1R01   Adverse Weather Protection (71111.01) ............................................................. 3
Enclosure
      1R04   Equipment Alignment (71111.04) ........................................................................ 4
TABLE OF CONTENTS SUMMARY OF FINDINGS ...........................................................................................................
      1R05   Fire Protection (71111.05) ................................................................................... 5
1 REPORT DETAILS ................................................................................................................
      1R06   Flooding (71111.06) ............................................................................................. 7
....... 3 Summary of Plant Status .......................................................................................................
      1R07   Annual Heat Sink Performance (71111.07) ......................................................... 7
.... 3 1. REACTOR SAFETY ....................................................................................................... 3
      1R07   Heat Sink Performance (71111.07T) ................................................................... 8
1R01 Adverse Weather Protection (71111.01) ............................................................. 3 1R04 Equipment Alignment (71111.04) ........................................................................ 4  
      1R12   Maintenance Effectiveness (71111.12) ............................................................. 15
1R05 Fire Protection (71111.05) ................................................................................... 5 1R06 Flooding (71111.06) ............................................................................................. 7 1R07 Annual Heat Sink Performance (71111.07) ......................................................... 7  
      1R13   Maintenance Risk Assessments and Emergent Work Control (71111.13) ........ 16
1R07 Heat Sink Performance (71111.07T) ................................................................... 8  
      1R15   Operability Evaluations (71111.15) .................................................................... 16
1R12 Maintenance Effectiveness (71111.12) ............................................................. 15 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ........ 16 1R15 Operability Evaluations (71111.15) .................................................................... 16  
      1R18   Plant Modifications (71111.18) .......................................................................... 17
1R18 Plant Modifications (71111.18) .......................................................................... 17  
      1R19   Post Maintenance Testing (71111.19) ............................................................... 18
1R19 Post Maintenance Testing (71111.19) ............................................................... 18  
  2.   RADIATION SAFETY ................................................................................................... 20
2. RADIATION SAFETY ................................................................................................... 20
      2RS1   Radiological Hazard Assessment and Exposure Controls (71124.01) .............. 20
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) .............. 20 2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06) ...................... 21  
      2RS6   Radioactive Gaseous and Liquid Effluent Treatment (71124.06) ...................... 21
4. OTHER ACTIVITIES (OA) ............................................................................................ 22
  4.   OTHER ACTIVITIES (OA) ............................................................................................ 22
4OA1 Performance Indicator Verification (71151) ....................................................... 22 4OA2 Identification and Resolution of Problems (71152) ............................................ 26  
      4OA1 Performance Indicator Verification (71151) ....................................................... 22
4OA3 Followup of Events and Notices of Enforcement Discretion (71153) ................. 28 4OA5 Other Activities ................................................................................................... 29 SUPPLEMENTAL INFORMATION ............................................................................................... 1
      4OA2   Identification and Resolution of Problems (71152) ............................................ 26
      4OA3   Followup of Events and Notices of Enforcement Discretion (71153) ................. 28
      4OA5   Other Activities ................................................................................................... 29
SUPPLEMENTAL INFORMATION ............................................................................................... 1
  KEY POINTS OF CONTACT..................................................................................................... 1
  KEY POINTS OF CONTACT..................................................................................................... 1
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 1
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 1
  LIST OF DOCUMENTS REVIEWED  
  LIST OF DOCUMENTS REVIEWED......................................................................................... 2
......................................................................................... 2
                                                                                                                        Enclosure
 
1 Enclosure  
SUMMARY OF FINDINGS
IR 05000454/2010005, 05000455/2010005; 07200068/2010003;
Byron Station, Units 1 & 2; 10/01/10 - 12/31/10; Routine Integrated Inspection Report; Heat Sink Performance; Operation of an Independent Spent Fuel Storage Installation at Operating Plants This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.  Two Severity Level IV Violations and one Green
finding were identified by the inspectors.  The Severity Level IV Violations and Green finding


were considered non-cited violations (NCVs) of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Assigned cross-cutting aspects were  
                                      SUMMARY OF FINDINGS
determined using IMC 0310, "Components Within the Cross Cutting Areas.Findings for which  
IR 05000454/2010005, 05000455/2010005; 07200068/2010003; Byron Station, Units 1 & 2;
the SDP does not apply may be Green or be assigned a severity level after NRC management  
10/01/10 - 12/31/10; Routine Integrated Inspection Report; Heat Sink Performance; Operation
review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reac
of an Independent Spent Fuel Storage Installation at Operating Plants
tor Oversight Process," Revision 4, dated December 2006. A. NRC-Identified and Self-Revealed Findings
This report covers a 3-month period of inspection by resident inspectors and announced
Cornerstone: Mitigating Systems  
baseline inspections by regional inspectors. Two Severity Level IV Violations and one Green
* Green. A finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," was identified by the inspectors when licensee personnel failed to establish specific  
finding were identified by the inspectors. The Severity Level IV Violations and Green finding
instructions for inspecting the River Screen House and Essential Service Water  
were considered non-cited violations (NCVs) of NRC regulations. The significance of most
findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter
(IMC) 0609, Significance Determination Process (SDP). Assigned cross-cutting aspects were
determined using IMC 0310, Components Within the Cross Cutting Areas. Findings for which
the SDP does not apply may be Green or be assigned a severity level after NRC management
review. The NRCs program for overseeing the safe operation of commercial nuclear power
reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated
December 2006.
A.     NRC-Identified and Self-Revealed Findings
        Cornerstone: Mitigating Systems
        *   Green. A finding of very low safety significance and an associated NCV of
            10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,
            was identified by the inspectors when licensee personnel failed to establish specific
            instructions for inspecting the River Screen House and Essential Service Water
            Cooling Tower. Specifically, the procedure that provided guidance for inspecting
            these structures lacked specific instructions on how to detect concrete degradation,
            erosion, corrosion and biological fouling. The licensee entered this issue into their
            corrective action program and initiated procedure revisions to provide further
            direction for identifying and documenting the degradation of these structures and
            related components.
            The performance deficiency was determined to be more than minor because if left
            uncorrected it would have the potential to lead to a more significant safety concern.
            The finding screened as of very low safety significance because it was a qualification
            deficiency confirmed not to result in a loss of operability or functionality. Specifically,
            a qualitative assessment of historic surveillance reports found the documented
            results acceptable. The inspectors determined that this finding did not represent
            current licensee performance and therefore no cross-cutting aspect was assigned.
            (Section 1R07.1)
        Miscellaneous Matters
        *    Severity Level IV: The inspectors identified a Severity Level IV NCV of very low
            safety significance of 10 CFR 72.150, "Instruction, Procedures, and Drawings."
            Specifically, the licensee failed to have procedures in place to ensure that the design
            basis peak fuel cladding limit would not be exceeded during canister loading
                                                1                                  Enclosure


Cooling Tower. Specifically, the procedure that provided guidance for inspecting these structures lacked specific instructions on how to detect concrete degradation, erosion, corrosion and biological fouling.  The licensee entered this issue into their  
      operations. The licensee entered this issue into their corrective action program and
corrective action program and initiated procedure revisions to provide further
      revised the procedure to provide monitoring criteria.
direction for identifying and documenting the degradation of these structures and
      The violation was determined to be of more than minor significance using IMC 0612,
related components. The performance deficiency was determined to be more than minor because if left uncorrected it would have the potential to lead to a more significant safety concern. The finding screened as of very low safety significance because it was a qualification
      Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues,
deficiency confirmed not to result in a loss of operability or functionality.  Specifically,
      Example 2c, in that the procedures failed to incorporate thermal acceptance criteria
a qualitative assessment of historic surveillance reports found the documented
      established by the Holtec Final Safety Analysis Report and that the failure to
results acceptable.  The inspectors determined that this finding did not represent current licensee performance and therefore no cross-cutting aspect was assigned. (Section 1R07.1)  
      incorporate thermal acceptance criteria was repetitive. Although the violation
Miscellaneous Matters
      contributed to the likelihood of peak fuel cladding temperatures exceeding the safety
* Severity Level IV: The inspectors identified a Severity Level IV NCV of very low safety significance of 10 CFR 72.150, "Instruction, Procedures, and Drawings." Specifically, the licensee failed to have procedures in place to ensure that the design
      limit, subsequent analysis by the licensee determined that fuel cladding temperature
basis peak fuel cladding limit would not be exceeded during canister loading 
      limits were not exceeded. The violation screened as having very low safety
2 Enclosure
      significance. (Section 4OA5.2)
operations. The licensee entered this issue into their corrective action program and revised the procedure to provide monitoring criteria. The violation was determined to be of more than minor significance using IMC 0612, "Power Reactor Inspection Reports," Appendix E, "Examples of Minor Issues,"
  * Severity Level IV: The inspectors identified a Severity Level IV NCV of very low
Example 2c, in that the procedures failed to incorporate thermal acceptance criteria established by the Holtec Final Safety Analysis Report and that the failure to incorporate thermal acceptance criteria was repetitive. Although the violation  
      safety significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings."
contributed to the likelihood of peak fuel cladding temperatures exceeding the safety  
      Specifically, the licensee failed to have procedures in place to ensure that heavy
limit, subsequent analysis by the licensee determined that fuel cladding temperature
      loads were operated safely in the Fuel Handling Building. The licensee entered this
      issue into their corrective action program and revised the procedure to provide
      monitoring criteria.
      The violation was determined to be of more than minor significance because if left
      uncorrected, it could lead to a more significant safety concern. Consistent with the
      guidance in Section 2.6.D of the NRC Enforcement Manual, if a violation does not fit
      an example in the Enforcement Policy Violation Examples, it should be assigned a
      severity level: (1) commensurate with its safety significance; and (2) informed by
      similar violations addressed in the Violation Examples. The violation screened as
      having very low safety significance. (Section 4OA5.2)
B. Licensee-Identified Violations
  None
                                          2                                Enclosure


limits were not exceeded.  The violation screened as having very low safety significance.  (Section 4OA5.2)
                                          REPORT DETAILS
* Severity Level IV:  The inspectors identified a Severity Level IV NCV of very low safety significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings."  Specifically, the licensee failed to have procedures in place to ensure that heavy
loads were operated safely in the Fuel Handling Building.  The licensee entered this
issue into their corrective action program and revised the procedure to provide monitoring criteria. The violation was determined to be of more than minor significance because if left uncorrected, it could lead to a more significant safety concern.  Consistent with the
guidance in Section 2.6.D of the NRC Enforcement Manual, if a violation does not fit an example in the Enforcement Policy Violation Examples, it should be assigned a severity level:  (1) commensurate with its safety significance; and (2) informed by
similar violations addressed in the Violation Examples.  The violation screened as
having very low safety significance.  (Section 4OA5.2) B. Licensee-Identified Violations
None 
 
 
 
 
3 Enclosure
REPORT DETAILS
 
Summary of Plant Status
Summary of Plant Status
Unit 1 operated at or near full power during the inspection period. Unit 2 operated at or near full power during the inspection period.  
Unit 1 operated at or near full power during the inspection period.
1. REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01) .2 Winter Seasonal Readiness Preparations
Unit 2 operated at or near full power during the inspection period.
a. Inspection Scope
1.   REACTOR SAFETY
The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather. Documentation for  
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather. During the inspection, the  
1R01 Adverse Weather Protection (71111.01)
inspectors focused on plant specific design features and the licensee's procedures used  
  .2     Winter Seasonal Readiness Preparations
to mitigate or respond to adverse weather conditions. Additionally, the inspectors  
  a.   Inspection Scope
reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant specific procedures. Cold weather protection, such as  
        The inspectors conducted a review of the licensees preparations for winter conditions to
heat tracing and area heaters, was verified to be in operation where applicable. The  
        verify that the plants design features and implementation of procedures were sufficient
inspectors also reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment to this report. The inspectors' reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues:  
        to protect mitigating systems from the effects of adverse weather. Documentation for
* Station Heating System (SH);  
        selected risk-significant systems was reviewed to ensure that these systems would
* Auxiliary Building Ventilation System (VA); and
        remain functional when challenged by inclement weather. During the inspection, the
* Essential Service Water Valve House Ventilation System (VH). This inspection constituted one winter seasonal readiness preparations sample as defined in Inspection Procedure (IP) 71111.01-05. b. Findings
        inspectors focused on plant specific design features and the licensees procedures used
No findings of significance were identified. 
        to mitigate or respond to adverse weather conditions. Additionally, the inspectors
4 Enclosure
        reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
.3 Readiness for Impending Adverse Weather Condition - Severe Thunderstorm Watch
        requirements for systems selected for inspection, and verified that operator actions were
and High Wind Conditions
        appropriate as specified by plant specific procedures. Cold weather protection, such as
   a. Inspection Scope
        heat tracing and area heaters, was verified to be in operation where applicable. The
Since thunderstorms with potential tornados and high winds were forecast in the vicinity of the facility on November 22, 2010, and high winds in the area on October 27, 2010,
        inspectors also reviewed corrective action program (CAP) items to verify that the
the inspectors reviewed the licensee's overall preparations/protection for the expected
        licensee was identifying adverse weather issues at an appropriate threshold and
weather conditions.  On October 27, 2010, and on November 19, 2010, the inspectors
        entering them into their CAP in accordance with station corrective action procedures.
walked down the plant outside areas, including the main transformers in addition to the
        Documents reviewed are listed in the Attachment to this report. The inspectors reviews
licensee's emergency alternating current (AC) power systems, because their safety-related functions could be affected or required as a result of high winds or tornado-generated missiles or the loss of offsite power.  The inspectors evaluated the
        focused specifically on the following plant systems due to their risk significance or
licensee staff's preparations against the site's procedures.  During the inspection, the
        susceptibility to cold weather issues:
inspectors focused on plant-specific design features and the licensee's procedures used
        *       Station Heating System (SH);
to respond to specified adverse weather conditions.  The inspectors also toured the plant grounds to look for any loose debris that could become missiles during a tornado.  The inspectors evaluated operator staffing and accessibility of controls and indications for
        *       Auxiliary Building Ventilation System (VA); and
those systems required to control the plant.  Additionally, the inspectors reviewed the
        *       Essential Service Water Valve House Ventilation System (VH).
UFSAR and performance requirements for systems selected for inspection, and verified
        This inspection constituted one winter seasonal readiness preparations sample as
that operator actions were appropriate as specified by plant specific procedures.  The inspectors also reviewed a sample of CAP items to verify that the licensee identified adverse weather issues at an appropriate threshold and dispositioned them through the
        defined in Inspection Procedure (IP) 71111.01-05.
CAP in accordance with station corrective action procedures.  Documents reviewed are listed in the Attachment to this report.  This inspection constituted two readiness for impending adverse weather condition samples as defined in IP 71111.01-05. b. Findings
  b.  Findings
No findings of significance were identified. 1R04 Equipment Alignment (71111.04) .1 Quarterly Partial System Walkdowns
        No findings of significance were identified.
a. Inspection Scope
                                                3                                 Enclosure
The inspectors performed partial system walkdowns of the following risk-significant systems: * Unit 1 Train A Centrifugal Charging and Safety Injection following Maintenance on the Room Cooler;
* Unit 1 Train A Emergency Diesel Generator (EDG) Air Start System during
Train B Maintenance Outage;
* Unit 1 Train A Containment Spray Valve Line-Up during  EDG Train B
Maintenance Outage;
* Unit 2 Train B Essential Service Water (SX) while Unit 2 Train A SX was Out of Service for Planned Maintenance; and 
5 Enclosure
* Unit 2 Train A Safety Injection (SI) while Unit 2 Train B SI was Out of Service for Planned Maintenance. The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected.  The inspectors attempted
to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
orders, condition reports, and the impact of ongoing work activities on redundant trains
of equipment in order to identify conditions that could have rendered the systems
incapable of performing their intended functions.  The inspectors also walked down
accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the components and observed operating parameter
s of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly
identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the
Attachment. These activities constituted five partial system walkdown samples as defined in
IP 71111.04-05. b. Findings
No findings of significance were identified. 1R05 Fire Protection (71111.05) .1 Routine Resident Inspector Tours (71111.05Q) a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk significant
plant areas:
* Auxiliary Building, Electrical Penetration Areas 426' and 414' Elevations (Fire
Zone 11.6-2, 11.5A-2 and 11.5B-2);
* Auxiliary Building, General Area 426' Elevation (Fire Zone 11.6-0 South);
* Auxiliary Building, General Area North 364' Elevation (Fire Zone 11.3-0 North);
* Unit 1 Train A Centrifugal Charging Pump Room (Fire Zone 11.3D-1); and
* Auxiliary Building, General Area North 383' Elevation (Fire Zone 11.4-0 North). The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained
passive fire protection features in good material condition, and implemented adequate
compensatory measures for out-of-service, degraded or inoperable fire protection
equipment, systems, or features in accordance with the licensee's fire plan.  The inspectors selected fire areas based on their overall contribution to internal fire risk as 
6 Enclosure  
documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a
plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that
fire detectors and sprinklers were unobstructed; that transient material loading was
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition.  The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.  Documents reviewed are
listed in the Attachment to this report.  These activities constituted five quarterly fire protection inspection samples as defined in
IP 71111.05-05. b. Findings
No findings of significance were identified. .2 Annual Fire Protection Drill Observation
(71111.05A) a. Inspection Scope
On October 20, 2010, the inspectors observed a fire brigade activation for a simulated
fire on the Unit 2 West Main Power Transformer, and on November 30, 2010, the
inspectors observed a portion of a fire brigade activation of a simulated fire in the Condensate Polisher Room.  Based on these observations, the inspectors evaluated the readiness of the plant fire brigade to fight fires.  The inspectors verified that the licensee
staff identified deficiencies; openly discussed them in a self-critical manner at the drill debrief, and took appropriate corrective actions.  Specific attributes evaluated were:
* proper wearing of turnout gear and self-contained breathing apparatus; 
* proper use and layout of fire hoses;
* employment of appropriate fire fighting techniques;
* sufficient firefighting equipment brought to the scene;
* effectiveness of fire brigade leader communications, command, and control;
* search for victims and propagation of the fire into other plant areas;
* smoke removal operations;
* utilization of pre-planned strategies;
* adherence to the pre-planned drill scenario; and
* drill objectives.  Documents reviewed are listed in the Attachment to this report. These activities constituted two annual fire protection inspection samples as defined in
IP 71111.05-05. b. Findings
No findings of significance were identified. 
7 Enclosure
1R06 Flooding (71111.06) .1 Internal Flooding
a. Inspection Scope
The inspectors reviewed selected risk important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal
flooding events.  The inspectors reviewed flood analyses and design documents,
including the UFSAR, engineering calculations, and abnormal operating procedures to
identify licensee commitments.  Documents reviewed are listed in the Attachment to this
report.  In addition, the inspectors reviewed licensee drawings to identify areas and equipment that may be affected by internal flooding caused by the failure or misalignment of nearby sources of water, such as the fire suppression or the circulating water systems.  The inspectors also reviewed the licensee's corrective action documents with respect to past flood-related items identified in the corrective action program to
verify the adequacy of the corrective actions.  The inspectors performed a walkdown of the following plant area to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and were operable, and that the licensee complied with its commitments:
* Flood Doors Associated with the Unit 1 Diesel Oil Storage Tank Rooms This inspection constituted one internal flooding sample as defined in IP 71111.06-05. b. Findings
No findings of significance were identified.  1R07 Annual Heat Sink Performance (71111.07) .1 Heat Sink Performance
a. Inspection Scope
The inspectors reviewed the licensee's testing of Unit 2 Train A SX Pump Oil Cooler and Cubicle Coolers to verify that potential deficiencies did not mask the licensee's ability to
detect degraded performance, to identify any common cause issues that had the
potential to increase risk, and to ensure that the licensee was adequately addressing problems that could result in initiating events that would cause an increase in risk.  The
inspectors reviewed the licensee's observations as compared against acceptance
criteria, the correlation of scheduled testing and the frequency of testing, and the impact
of instrument inaccuracies on test results.  The inspectors also verified that test acceptance criteria considered differences between test conditions, design conditions, and testing conditions.  Documents reviewed are listed in the Attachment to this report. This annual heat sink performance inspection constituted one sample as defined in
IP 71111.07-05. 
8 Enclosure
b. Findings
No findings of significance were identified. 1R07 Heat Sink Performance (71111.07T) .1 Triennial Review of Heat Sink Performance
a. Inspection Scope
The inspectors reviewed operability determinations, completed surveillances, vendor manual information, associated calculations, performance test results and
cooler inspection results associated with the 1A EDG jacket water cooler and 1B


auxiliary feed pump oil cooler. These heat exchangers/coolers were chosen based on their risk-significance in the licensee's probabilistic safety analysis, their important safety-related mitigating system support functions, their operating history, and their
  .3  Readiness for Impending Adverse Weather Condition - Severe Thunderstorm Watch
relatively low margin. For the1A EDG jacket water cooler and the 1B auxiliary feed pump oil cooler the inspectors verified the methods used to inspect and clean heat exchangers were
      and High Wind Conditions
consistent with as-found conditions identified and expected degradation trends and  
  a. Inspection Scope
industry standards.  The inspectors verified the licensee's inspection and cleaning
      Since thunderstorms with potential tornados and high winds were forecast in the vicinity
activities utilized acceptance criteria generated via methods consistent with industry standards, and that the as-found results were recorded, evaluated, and appropriately dispositioned.  The inspectors also verified that the corrective actions program contained guidance requiring characterization and evaluation of any foreign materials identified in
      of the facility on November 22, 2010, and high winds in the area on October 27, 2010,
the heat exchanger.  The inspectors confirmed evaluations were performed to ensure
      the inspectors reviewed the licensees overall preparations/protection for the expected
the heat exchanger would remain capable of performing its intended design function. 
      weather conditions. On October 27, 2010, and on November 19, 2010, the inspectors
The licensee initiated action-tracking items to generate heat exchanger specific tube plugging and blocking calculations as an enhancement to the heat exchanger monitoring
      walked down the plant outside areas, including the main transformers in addition to the
program for the 1B AF lube oil cooler. In addition, the inspectors verified the condition and operation of the 1A EDG jacket water cooler and the 1B AF pump oil cooler were consistent with design assumptions in
      licensees emergency alternating current (AC) power systems, because their
heat transfer calculations and Proto HX calculations and as described in the UFSAR. 
      safety-related functions could be affected or required as a result of high winds or
This included verification that the number of plugged tubes was within pre-established
      tornado-generated missiles or the loss of offsite power. The inspectors evaluated the
limits based on capacity and heat transfer assumptions.  In addition, eddy current test reports and visual inspection records were reviewed to determine the structural integrity of the heat exchanger. The inspectors verified the performance of ultimate heat sinks (UHSs) and safety-related service water systems and their subcomponents such as piping, intake screens, pumps, valves, etc., by tests or other equivalent methods to ensure availability and accessibility to the in-plant cooling water systems. The inspectors reviewed the results of the licensee's inspection of the UHS and the River Screen House (RSH).  At Byron, the UHS is comprised of the essential service water cooling tower (SXCT) basin. The inspectors verified that identified settlement or movement indicating a potential loss of structural integrity was appropriately evaluated and dispositioned by the licensee.  The inspectors also performed walkdowns of 
      licensee staffs preparations against the sites procedures. During the inspection, the
9 Enclosure
      inspectors focused on plant-specific design features and the licensees procedures used
accessible portions of components in the SXCT basin to verify the licensee's assessment on structural integrity and component functionality.   The inspectors verified that the licensee's inspection of the SXCT basin and the RSH was comprehensive and of significant depth.  The inspectors also verified the licensee
      to respond to specified adverse weather conditions. The inspectors also toured the plant
ensured sufficient reservoir capacity by trending and removing debris and sediment buildup.  In addition, the inspectors confirmed that sediments were maintained at an acceptable level and that water level instruments were functional and routinely
      grounds to look for any loose debris that could become missiles during a tornado. The
monitored in the UHS.  This included the review of the licensee's periodic monitoring and trending of sediment build-up and heat transfer capability calculations.  The inspectors verified the licensee's ability to ensure functionality during adverse weather conditions. The inspectors also verified that the licensee had adequately protected against silt introduction during periods of low flow or low level. The inspectors reviewed available licensee testing and inspections results, licensee disposition of any active thru wall pipe leaks, and the history of thru wall pipe leakage to  
      inspectors evaluated operator staffing and accessibility of controls and indications for
identify any adverse trends since the last
      those systems required to control the plant. Additionally, the inspectors reviewed the
NRC inspection. For the chemical volume control system, a closed-cooling system, the inspectors reviewed related documents and  
      UFSAR and performance requirements for systems selected for inspection, and verified
interviewed the system engineer, to identify adverse make-up trends that could be
      that operator actions were appropriate as specified by plant specific procedures. The
indicative of excessive leakage out of the closed system. For inaccessible piping, the
      inspectors also reviewed a sample of CAP items to verify that the licensee identified
inspectors reviewed the licensee's pipe testing, inspection, or monitoring program to verify structural integrity, and ensured that any leakage or degradation has been appropriately identified and dispositioned by the licensee. The inspectors verified that
      adverse weather issues at an appropriate threshold and dispositioned them through the
the periodic piping inspection program adequately detected and corrected protective
      CAP in accordance with station corrective action procedures. Documents reviewed are
coating failure, corrosion and erosion.  The inspectors verified that the licensee
      listed in the Attachment to this report.
      This inspection constituted two readiness for impending adverse weather condition
      samples as defined in IP 71111.01-05.
  b. Findings
      No findings of significance were identified.
1R04 Equipment Alignment (71111.04)
  .1  Quarterly Partial System Walkdowns
  a. Inspection Scope
      The inspectors performed partial system walkdowns of the following risk-significant
      systems:
      *        Unit 1 Train A Centrifugal Charging and Safety Injection following Maintenance
              on the Room Cooler;
      *        Unit 1 Train A Emergency Diesel Generator (EDG) Air Start System during
              Train B Maintenance Outage;
      *        Unit 1 Train A Containment Spray Valve Line-Up during EDG Train B
              Maintenance Outage;
      *        Unit 2 Train B Essential Service Water (SX) while Unit 2 Train A SX was Out of
              Service for Planned Maintenance; and
                                            4                                  Enclosure


adequately monitored and resolved any adverse trends for pumps by reviewing the operational history and in-service testing (IST) vibration monitoring results. In addition, the inspectors reviewed condition reports related to the heat exchangers and heat sink performance issues to verify that the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. Documents reviewed are listed in the Attachment to this report.   These inspection activities constituted three heat sink inspection samples as defined in  
      *        Unit 2 Train A Safety Injection (SI) while Unit 2 Train B SI was Out of Service for
IP 71111.07-05. b. Findings
                Planned Maintenance.
(1) Inadequate Instructions for the Inspection of the River Screen House and Essential
      The inspectors selected these systems based on their risk significance relative to the
Service Water Cooling Tower
      Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
  Introduction:  A finding of very low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings," was
      to identify any discrepancies that could impact the function of the system, and, therefore,
identified by the inspectors when licensee personnel failed to establish specific
      potentially increase risk. The inspectors reviewed applicable operating procedures,
instructions for inspecting the RSH and SXCT.  Specifically, the procedure that provided guidance for inspecting these structures lacked specific instructions on how to detect concrete degradation, erosion, corrosion and biological fouling.
      system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
Description:  On November 24, 2010, the inspectors identified that the licensee failed to establish adequate instructions in surveillance procedures used to inspect the RSH and SXCT. 
      orders, condition reports, and the impact of ongoing work activities on redundant trains
10 Enclosure
      of equipment in order to identify conditions that could have rendered the systems
In response to Generic Letter (GL) 89-13, "Service Water Problems Affecting Safety-Related Equipment," the licensee committed to inspect the RSH and the SXCT
      incapable of performing their intended functions. The inspectors also walked down
basin to monitor, trend and evaluate any degradation resulting from erosion, corrosion, silt buildup and biological fouling. The purpose section of procedure 0BMSR SX-5, "Inspection of River Screen House and Essential Service Water Cooling Tower Basins (CM-4)," states:  "This procedure provides guidance for inspection of River Screen House (RSH) Intake Structure and the
      accessible portions of the systems to verify system components and support equipment
Essential Service Water Cooling Tower (SXCT) Basins for concrete degradation, silt
      were aligned correctly and operable. The inspectors examined the material condition of
buildup, erosion, corrosion, and biological fouling."  However, the inspectors noted the
      the components and observed operating parameters of equipment to verify that there
procedure did not include specific guidance on how to accomplish this purpose.  For example, the inspectors noted the procedure contained Step 4.2.3, which required inspection of the SX makeup pump, but did not provide guidance on how to accomplish
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
it or what specific sections of the pump and the basins to inspect.  In addition, the  
      identified and resolved equipment alignment problems that could cause initiating events
procedure did not provide any instructions for what entails degradation of concrete
      or impact the capability of mitigating systems or barriers and entered them into the CAP
structures or components by erosion, corrosion and biological fouling mechanisms.  In
      with the appropriate significance characterization. Documents reviewed are listed in the
addition, the procedure did not provide instructions on when or how to document these types of degradations.  The inspectors were concerned that the lack of written instructions to identify and record the as-found condition of the RSH and the SXCT basin
      Attachment.
could result in the licensee's inability to properly assess the effect of erosion, corrosion, biological fouling and concrete degradation on these structures and related components.  As a corrective action, the licensee initiated Issue Report (IR) 1144584 to revise Procedure 0BMSR SX-5, and provide specific instructions on how to accomplish the
      These activities constituted five partial system walkdown samples as defined in
purpose of the procedure.  These instructions will include criteria for what to look for and how and what to document during these inspections related to component and structural degradation by erosion, corrosion and biological fouling.
      IP 71111.04-05.
Analysis:  The inspectors determined that the licensee's failure to establish adequate instructions in surveillance procedures used to inspect the RSH and SXCT was contrary
    b. Findings
to the requirements of 10 CFR Part 50, Appendix B, Criterion V, and was a performance deficiency. The performance deficiency was determined to be more than minor because if left uncorrected it would have the potential to lead to a more significant safety concern. 
      No findings of significance were identified.
Specifically, since the licensee's procedures did not contain instructions to properly inspect the RSH and SXCT, the potential existed for an unacceptable degradation of these structures or related components to go undetected affecting essential service
1R05 Fire Protection (71111.05)
water operability.  Inoperable essential service water trains would place the plant at increased risk for core damage, which would affect the safety of an operating reactor. The inspectors determined the finding could be evaluated using the Significance Determination Process (SDP) in accordance with IMC 0609, "Significance Determination
  .1    Routine Resident Inspector Tours (71111.05Q)
Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a for the Mitigating System Cornerstone. The finding screened as of very low safety significance (Green) because the finding was a qualification deficiency
    a. Inspection Scope
confirmed not to result in a loss of operability or functionality.  Specifically, the licensee
      The inspectors conducted fire protection walkdowns which were focused on availability,
performed a history review of the surveillance reports and found the documented results
      accessibility, and the condition of firefighting equipment in the following risk significant
acceptable.  A qualitative assessment of the inspections established reasonable
      plant areas:
assurance that they did not represent a loss of operability.  The inspectors did not have
      *        Auxiliary Building, Electrical Penetration Areas 426' and 414' Elevations (Fire
                Zone 11.6-2, 11.5A-2 and 11.5B-2);
      *        Auxiliary Building, General Area 426' Elevation (Fire Zone 11.6-0 South);
      *        Auxiliary Building, General Area North 364 Elevation (Fire Zone 11.3-0 North);
      *        Unit 1 Train A Centrifugal Charging Pump Room (Fire Zone 11.3D-1); and
      *        Auxiliary Building, General Area North 383 Elevation (Fire Zone 11.4-0 North).
      The inspectors reviewed areas to assess if the licensee had implemented a fire
      protection program that adequately controlled combustibles and ignition sources within
      the plant, effectively maintained fire detection and suppression capability, maintained
      passive fire protection features in good material condition, and implemented adequate
      compensatory measures for out-of-service, degraded or inoperable fire protection
      equipment, systems, or features in accordance with the licensees fire plan. The
      inspectors selected fire areas based on their overall contribution to internal fire risk as
                                                5                                  Enclosure


further concerns. 
    documented in the plants Individual Plant Examination of External Events with later
11 Enclosure
    additional insights, their potential to impact equipment which could initiate or mitigate a
The inspectors determined that this finding did not represent current licensee performance and therefore no cross-cutting aspect was assigned.
    plant transient, or their impact on the plants ability to respond to a security event. Using
Enforcement:  Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," required, in part, that activities affecting quality shall be prescribed by
    the documents listed in the Attachment, the inspectors verified that fire hoses and
documented instructions, procedures, or drawings, of a type appropriate to the  
    extinguishers were in their designated locations and available for immediate use; that
circumstances. Contrary to the above, as of November 24, 2010, the licensee did not establish RSH and SXCT basin surveillance procedural requirements appropriate to the circumstances.  Specifically, procedure 0BMSR SX-5, "Inspection of River Screen House and Essential
    fire detectors and sprinklers were unobstructed; that transient material loading was
Service Water Cooling Tower Basins (CM-4)," the procedure used to inspect these
    within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
structures, was not appropriate for the circumstances.  The procedure lacked
    be in satisfactory condition. The inspectors also verified that minor issues identified
instructions on detecting or recording concrete degradation, erosion, corrosion and biological fouling.  Without these instructions, the effect of any degradation on system operability could not be evaluated.  Because this violation was of very low safety
    during the inspection were entered into the licensees CAP. Documents reviewed are
significance and it was entered into the licensee's CAP as IR 1144584, this violation is
    listed in the Attachment to this report.
being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000454/2010005-01; 05000455/2010005-01, Inadequate Instructions for the Inspection of the River Screen House and Essential Service Water Cooling Tower)
    These activities constituted five quarterly fire protection inspection samples as defined in
1R11 Licensed Operator Requalification Program (71111.11) .1 Facility Operating History (71111.11B) a. Inspection Scope
    IP 71111.05-05.
The inspectors reviewed the plant's operating history from October 26 through October 27, 2010, to identify operating experience that was expected to be addressed by the Licensed Operator Requalification Training (LORT) program. The inspector
  b. Findings
verified that the identified operating experience had been addressed by the facility
    No findings of significance were identified.
licensee in accordance with the station's approved Systems Approach to Training (SAT) program to satisfy the requirements of 10 CFR 55.59(c).  Documents reviewed are listed  
.2  Annual Fire Protection Drill Observation (71111.05A)
in the Attachment to this report.  b. Findings
No findings of significance were identified. .2 Licensee Requalification Examinations
a. Inspection Scope
The inspectors performed an inspection of the licensee's LORT test/examination program for compliance with the station's SAT program which would satisfy the
requirements of 10 CFR 55.59(c)(4).  The reviewed operating examination material  
consisted of two operating tests, each containing two dynamic simulator scenarios and
six job performance measures (JPMs).  The written examinations reviewed consisted of two written examinations; each exam contained 30 questions.  The inspectors reviewed the annual requalification operating test and biennial written examination material to
evaluate general quality, construction, and difficulty level. The inspectors assessed the 
12 Enclosure
level of examination material duplication fr
om week-to-week during the current year operating test.  The examiners assessed the amount of written examination material duplication from week-to-week for the written examination administered in 2010.  The inspectors reviewed the methodology for developing the examinations, including the LORT program 2-year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications. Documents reviewed are listed in the Attachment to this report.   b. Findings
No findings of significance were identified. .3 Licensee Administration of Requalification Examinations
a. Inspection Scope
The inspectors observed the administration of a requalification operating test to assess the licensee's effectiveness in conducting the test to ensure compliance with 10 CRF 55.59(c)(4).  The inspectors evaluated the performance of two crews in parallel
with the facility evaluators during two dynamic simulator scenarios and evaluated various
licensed crew members concurrently with facility evaluators during the administration of
several JPMs. The inspectors assessed the facility evaluators' ability to determine
adequate crew and individual performance using objective, measurable standards.  The inspectors observed the training staff personnel administer the operating test, including conducting pre-examination briefings, evaluations of operator performance, and
individual and crew evaluations upon completion of the operating test. The inspectors
evaluated the ability of the simulator to support the examinations.  A specific evaluation
of simulator performance was conducted and documented in the section below titled, "Conformance with Simulator Requirements Specified in 10 CFR 55.46." Documents reviewed are listed in the Attachment to this report.  b. Findings
No findings of significance were identified. .4 Examination Security
  a. Inspection Scope
  a. Inspection Scope
The inspectors observed and reviewed the licensee's overall licensed operator requalification examination security program related to examination physical security (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability and bias) to verify compliance with 10 CFR 55.49, "Integrity of Examinations and Tests.The inspectors also reviewed the facility licensee's examination security procedure, any corrective actions related to past or present examination security problems at the facility, and the implementation of security and integrity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition) throughout the examination process.  Documents reviewed are listed in the Attachment to this report.  
    On October 20, 2010, the inspectors observed a fire brigade activation for a simulated
13 Enclosure
    fire on the Unit 2 West Main Power Transformer, and on November 30, 2010, the
    inspectors observed a portion of a fire brigade activation of a simulated fire in the
    Condensate Polisher Room. Based on these observations, the inspectors evaluated the
    readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee
    staff identified deficiencies; openly discussed them in a self-critical manner at the drill
    debrief, and took appropriate corrective actions. Specific attributes evaluated were:
    *        proper wearing of turnout gear and self-contained breathing apparatus;
    *        proper use and layout of fire hoses;
    *        employment of appropriate fire fighting techniques;
    *        sufficient firefighting equipment brought to the scene;
    *        effectiveness of fire brigade leader communications, command, and control;
    *        search for victims and propagation of the fire into other plant areas;
    *        smoke removal operations;
    *        utilization of pre-planned strategies;
    *        adherence to the pre-planned drill scenario; and
    *        drill objectives.
    Documents reviewed are listed in the Attachment to this report.
    These activities constituted two annual fire protection inspection samples as defined in
    IP 71111.05-05.
  b. Findings
  b. Findings
No findings of significance were identified. .5 Licensee Training Feedback System
    No findings of significance were identified.
a. Inspection Scope
                                            6                                  Enclosure
The inspectors assessed the methods and effectiveness of the licensee's processes for revising and maintaining its LORT Program up to date, including the use of feedback
from plant events and industry experience information.  The inspectors reviewed the licensee's quality assurance oversight activities, including licensee training department self-assessment reports.  The inspectors evaluated the licensee's ability to assess the


effectiveness of its LORT program and their ability to implement appropriate corrective actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and the licensee's SAT program.  Documents reviewed are listed in the Attachment to this
1R06 Flooding (71111.06)
report.  b. Findings
  .1    Internal Flooding
  No findings of significance were identified. .6 Licensee Remedial Training Program
    a. Inspection Scope
a. Inspection Scope
        The inspectors reviewed selected risk important plant design features and licensee
The inspectors assessed the adequacy and effectiveness of the remedial training conducted since the previous biennial requalification examinations and the training from the current examination cycle to ensure that they addressed weaknesses in licensed operator or crew performance identified during training and plant operations. The  
        procedures intended to protect the plant and its safety-related equipment from internal
inspectors reviewed remedial training procedur
        flooding events. The inspectors reviewed flood analyses and design documents,
es and individual remedial training plans.  This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to  
        including the UFSAR, engineering calculations, and abnormal operating procedures to
the licensee's SAT program. Documents reviewed are listed in the Attachment to this  
        identify licensee commitments. Documents reviewed are listed in the Attachment to this
report.   b. Findings
        report. In addition, the inspectors reviewed licensee drawings to identify areas and
No findings of significance were identified. .7 Conformance with Operator License Conditions
        equipment that may be affected by internal flooding caused by the failure or
a. Inspection Scope
        misalignment of nearby sources of water, such as the fire suppression or the circulating
The inspectors reviewed the facility and individual operator licensees' conformance with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's
        water systems. The inspectors also reviewed the licensees corrective action documents
program for maintaining active operator licenses and to assess compliance with
        with respect to past flood-related items identified in the corrective action program to
10 CFR 55.53(e) and (f).  The inspectors reviewed the procedural guidance and the
        verify the adequacy of the corrective actions. The inspectors performed a walkdown of
process for tracking on-shift hours for licensed operators and which control room positions were granted watch-standing credit for maintaining active operator licenses.  The inspectors reviewed the facility licensee's LORT program to assess compliance with  
        the following plant area to assess the adequacy of watertight doors and verify drains and
the requalification program requirements as described by 10 CFR 55.59(c).  Additionally, medical records for 10 licensed operators were reviewed for compliance with 
        sumps were clear of debris and were operable, and that the licensee complied with its
14 Enclosure
        commitments:
10 CFR 55.21 and 55.53(i).  Documents reviewed are listed in the Attachment to this
        *        Flood Doors Associated with the Unit 1 Diesel Oil Storage Tank Rooms
report.  b. Findings
        This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
No findings of significance were identified. .8 Conformance with Simulator Requirements Specified in 10 CFR 55.46
    b. Findings
a. Inspection Scope
        No findings of significance were identified.
The inspectors assessed the adequacy of the licensee's simulation facility (simulator) for use in operator licensing examinations and for satisfying experience requirements as prescribed in 10 CFR 55.46, "Simulation Facilities."  The inspectors also reviewed a
1R07 Annual Heat Sink Performance (71111.07)
sample of simulator performance test records (i.e., transient tests, malfunction tests,  
.1    Heat Sink Performance
steady state tests, and core performance tests), simulator discrepancies, and the  
    a. Inspection Scope
process for ensuring continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to ensure that simulator fidelity was maintained.  Open simulator discrepancies were
        The inspectors reviewed the licensees testing of Unit 2 Train A SX Pump Oil Cooler and
reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator
        Cubicle Coolers to verify that potential deficiencies did not mask the licensees ability to
actions as well as on nuclear and thermal hydraulic operating characteristics. The  
        detect degraded performance, to identify any common cause issues that had the
inspectors conducted interviews with members of the licensee's simulator staff about the
        potential to increase risk, and to ensure that the licensee was adequately addressing
configuration control process and completed the IP 71111.11, Appendix C, checklist to evaluate whether or not the licensee's plant-referenced simulator was operating adequately as required by 10 CFR 55.46(c) and (d). Documents reviewed are listed in the Attachment to this report.   b. Findings
        problems that could result in initiating events that would cause an increase in risk. The
No findings of significance were identified. .9 Resident Inspector Quarterly Review (71111.11Q) a. Inspection Scope
        inspectors reviewed the licensees observations as compared against acceptance
On October 26 and October 27, 2010, the inspectors observed two crews of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in
        criteria, the correlation of scheduled testing and the frequency of testing, and the impact
accordance with licensee procedures.  The inspectors evaluated the following areas:
        of instrument inaccuracies on test results. The inspectors also verified that test
        acceptance criteria considered differences between test conditions, design conditions,
        and testing conditions. Documents reviewed are listed in the Attachment to this report.
        This annual heat sink performance inspection constituted one sample as defined in
        IP 71111.07-05.
                                                7                                  Enclosure


  * licensed operator performance;
    b. Findings
* crew's clarity and formality of communications;
      No findings of significance were identified.
* ability to take timely actions in the conservative direction;
1R07 Heat Sink Performance (71111.07T)
* prioritization, interpretation, and verification of annunciator alarms;
  .1    Triennial Review of Heat Sink Performance
* correct use and implementation of abnormal and emergency procedures;
    a. Inspection Scope
* control board manipulations;
      The inspectors reviewed operability determinations, completed surveillances,
* oversight and direction from supervisors; and  
      vendor manual information, associated calculations, performance test results and
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.  
      cooler inspection results associated with the 1A EDG jacket water cooler and 1B
 
      auxiliary feed pump oil cooler. These heat exchangers/coolers were chosen based
15 Enclosure
      on their risk-significance in the licensees probabilistic safety analysis, their important
The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed  
      safety-related mitigating system support functions, their operating history, and their
are listed in the Attachment to this report.  
      relatively low margin.
This inspection constituted one quarterly licensed operator requalification program
      For the1A EDG jacket water cooler and the 1B auxiliary feed pump oil cooler the
sample as defined in IP 71111.11-05.  
      inspectors verified the methods used to inspect and clean heat exchangers were
      consistent with as-found conditions identified and expected degradation trends and
      industry standards. The inspectors verified the licensees inspection and cleaning
      activities utilized acceptance criteria generated via methods consistent with industry
      standards, and that the as-found results were recorded, evaluated, and appropriately
      dispositioned. The inspectors also verified that the corrective actions program contained
      guidance requiring characterization and evaluation of any foreign materials identified in
      the heat exchanger. The inspectors confirmed evaluations were performed to ensure
      the heat exchanger would remain capable of performing its intended design function.
      The licensee initiated action-tracking items to generate heat exchanger specific tube
      plugging and blocking calculations as an enhancement to the heat exchanger monitoring
      program for the 1B AF lube oil cooler.
      In addition, the inspectors verified the condition and operation of the 1A EDG jacket
      water cooler and the 1B AF pump oil cooler were consistent with design assumptions in
      heat transfer calculations and Proto HX calculations and as described in the UFSAR.
      This included verification that the number of plugged tubes was within pre-established
      limits based on capacity and heat transfer assumptions. In addition, eddy current test
      reports and visual inspection records were reviewed to determine the structural integrity
      of the heat exchanger.
      The inspectors verified the performance of ultimate heat sinks (UHSs) and safety-related
      service water systems and their subcomponents such as piping, intake screens, pumps,
      valves, etc., by tests or other equivalent methods to ensure availability and accessibility
      to the in-plant cooling water systems.
      The inspectors reviewed the results of the licensees inspection of the UHS and the
      River Screen House (RSH). At Byron, the UHS is comprised of the essential service
      water cooling tower (SXCT) basin. The inspectors verified that identified settlement or
      movement indicating a potential loss of structural integrity was appropriately evaluated
      and dispositioned by the licensee. The inspectors also performed walkdowns of
                                              8                                    Enclosure


b. Findings
    accessible portions of components in the SXCT basin to verify the licensees
No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12) .1 Routine Quarterly Evaluations (71111.12Q) a. Inspection Scope
    assessment on structural integrity and component functionality.
The inspectors evaluated degraded performance issues involving the following risk-significant systems:
    The inspectors verified that the licensees inspection of the SXCT basin and the RSH
* Failure of Unit 2 Train A EDG Upper Lube Oil Cooler Fixed End Flange Connection. The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and
    was comprehensive and of significant depth. The inspectors also verified the licensee
independently verified the licensee's actions to address system performance or condition problems in terms of the following:
    ensured sufficient reservoir capacity by trending and removing debris and sediment
* implementing appropriate work practices;
    buildup. In addition, the inspectors confirmed that sediments were maintained at an
* identifying and addressing common cause failures;
    acceptable level and that water level instruments were functional and routinely
* scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
    monitored in the UHS. This included the review of the licensees periodic monitoring and
* characterizing system reliability issues for performance;
    trending of sediment build-up and heat transfer capability calculations.
* charging unavailability for performance;
    The inspectors verified the licensees ability to ensure functionality during adverse
* trending key parameters for condition monitoring;
    weather conditions. The inspectors also verified that the licensee had adequately
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  
    protected against silt introduction during periods of low flow or low level.
* verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1). The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system.  In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly maintenance effectiveness samples as defined in IP 71111.12-05. b. Findings
    The inspectors reviewed available licensee testing and inspections results, licensee
No findings of significance were documented in this inspection report.  Additional follow-up and regulatory conclusions are the subject of NRC IR 05000455/2011011.
    disposition of any active thru wall pipe leaks, and the history of thru wall pipe leakage to
16 Enclosure
    identify any adverse trends since the last NRC inspection. For the chemical volume
1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) .1 Maintenance Risk Assessments and Emergent Work Control
    control system, a closed-cooling system, the inspectors reviewed related documents and
a. Inspection Scope
    interviewed the system engineer, to identify adverse make-up trends that could be
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related
    indicative of excessive leakage out of the closed system. For inaccessible piping, the
equipment listed below to verify that the appropriate risk assessments were performed
    inspectors reviewed the licensee's pipe testing, inspection, or monitoring program to
prior to removing equipment for work:
    verify structural integrity, and ensured that any leakage or degradation has been
* Work Activities during the Week of November 8 Focusing on Unit 2 Train A SX
    appropriately identified and dispositioned by the licensee. The inspectors verified that
Outage; and  
    the periodic piping inspection program adequately detected and corrected protective
* Work Activities during the Week of November 29 for Unit 1 Emergent Direct
    coating failure, corrosion and erosion. The inspectors verified that the licensee
Current (DC) Bus 112 Battery Cell Replacement and Planned Unit 2 Safety Injection Pump work window.  These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the  
    adequately monitored and resolved any adverse trends for pumps by reviewing the
plant risk was promptly reassessed and managed. The inspectors reviewed the scope
    operational history and in-service testing (IST) vibration monitoring results.
of maintenance work, discussed the results of the assessment with the licensee's
    In addition, the inspectors reviewed condition reports related to the heat exchangers and
probabilistic risk analyst or shift technical advisor, and verified plant conditions were
    heat sink performance issues to verify that the licensee had an appropriate threshold for
consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. These maintenance risk assessments and emergent work control activities constituted  
    identifying issues and to evaluate the effectiveness of the corrective actions. Documents
two samples as defined in IP 71111.13-05. b. Findings
    reviewed are listed in the Attachment to this report.
No findings of significance were identified. 1R15 Operability Evaluations (71111.15) .1 Operability Evaluations
    These inspection activities constituted three heat sink inspection samples as defined in
a. Inspection Scope
    IP 71111.07-05.
The inspectors reviewed the following issues:
b. Findings
* Unit 2 Train A Pressurizer Safety Valve Due to Identified but Unexpected Leakby;
(1) Inadequate Instructions for the Inspection of the River Screen House and Essential
* Unit 2 Train A SX Foreign Material Discovered within the Lube Oil Pump; and  
    Service Water Cooling Tower
* Unit 1 Train B Auxiliary Feedwater Pump Oil Cooler Piping Configuration Error. The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the
    Introduction: A finding of very low safety significance (Green) and an associated NCV of
subject component or system remained available such that no unrecognized increase in 
    10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, was
17 Enclosure
    identified by the inspectors when licensee personnel failed to establish specific
risk occurred.  The inspectors compared the operability and design criteria in the appropriate sections of the TS and USAR to the licensee's evaluations to determine
    instructions for inspecting the RSH and SXCT. Specifically, the procedure that provided
    guidance for inspecting these structures lacked specific instructions on how to detect
    concrete degradation, erosion, corrosion and biological fouling.
    Description: On November 24, 2010, the inspectors identified that the licensee failed to
    establish adequate instructions in surveillance procedures used to inspect the RSH and
    SXCT.
                                          9                                    Enclosure


whether the components or systems were
In response to Generic Letter (GL) 89-13, Service Water Problems Affecting
operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled.  The inspectors
Safety-Related Equipment, the licensee committed to inspect the RSH and the SXCT
determined, where appropriate, compliance with bounding limitations associated with the
basin to monitor, trend and evaluate any degradation resulting from erosion, corrosion,
evaluations. Additionally, the inspectors reviewed a sampling of corrective action
silt buildup and biological fouling.
documents to verify that the licensee was identifying and correcting any deficiencies
The purpose section of procedure 0BMSR SX-5, Inspection of River Screen House and
associated with operability evaluations.  Documents reviewed are listed in the
Essential Service Water Cooling Tower Basins (CM-4), states: This procedure
Attachment to this report. This operability inspection constituted three samples as defined in IP 71111.15-05. b. Findings
provides guidance for inspection of River Screen House (RSH) Intake Structure and the
No findings of significance were identified. 1R18 Plant Modifications (71111.18) .1 Temporary Plant Modifications
Essential Service Water Cooling Tower (SXCT) Basins for concrete degradation, silt
a. Inspection Scope
buildup, erosion, corrosion, and biological fouling. However, the inspectors noted the
The inspectors reviewed the following temporary modifications:
procedure did not include specific guidance on how to accomplish this purpose. For
* Unit 2 Temporarily Disconnect Both Sudden Pressure Relays for Main Power Transformer 2MP01E due to Ground Associated with Relay 63-1; and
example, the inspectors noted the procedure contained Step 4.2.3, which required
* Unit 1 Battery Bank 112 Installation of Jumper for Degraded Cell. The inspectors compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TS, as applicable, to verify that the modification did not affect the
inspection of the SX makeup pump, but did not provide guidance on how to accomplish
operability or availability of the affected system(s). The inspectors also compared the
it or what specific sections of the pump and the basins to inspect. In addition, the
licensee's information to operating experience information to ensure that lessons learned
procedure did not provide any instructions for what entails degradation of concrete
from other utilities had been incorporated into the licensee's decision to implement the
structures or components by erosion, corrosion and biological fouling mechanisms. In
temporary modification. The inspectors, as applicable, performed field verifications to ensure that the modifications were installed as directed; the modifications operated as expected; modification testing adequately demonstrated continued system operability,
addition, the procedure did not provide instructions on when or how to document these
availability, and reliability; and that operation of the modifications did not impact the  
types of degradations. The inspectors were concerned that the lack of written
operability of any interfacing systems.  Lastly, the inspectors discussed the temporary
instructions to identify and record the as-found condition of the RSH and the SXCT basin
modification with operations, engineering, and training personnel to ensure that the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance.
could result in the licensees inability to properly assess the effect of erosion, corrosion,
  Documents reviewed are listed in the Attachment to this report.  This inspection constituted two temporary modification samples as defined in
biological fouling and concrete degradation on these structures and related components.
IP 71111.18-05. b. Findings
As a corrective action, the licensee initiated Issue Report (IR) 1144584 to revise
No findings of significance were identified.
Procedure 0BMSR SX-5, and provide specific instructions on how to accomplish the
18 Enclosure
purpose of the procedure. These instructions will include criteria for what to look for and
1R19 Post Maintenance Testing (71111.19)  .1 Post Maintenance Testing
how and what to document during these inspections related to component and structural
a. Inspection Scope
degradation by erosion, corrosion and biological fouling.
The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
Analysis: The inspectors determined that the licensees failure to establish adequate
* Unit 1 Train A Chemical Volume Control Pump Room Cooling Fan Following Motor Replacement;
instructions in surveillance procedures used to inspect the RSH and SXCT was contrary
* Unit 1 Train B EDG Following Planned Maintenance Work Window;
to the requirements of 10 CFR Part 50, Appendix B, Criterion V, and was a performance
* Unit 1 Battery Bank 112 Installation of Jumper for Degraded Cell;
deficiency.
* Unit 2 Train B Auxiliary Feedwater Pump Following Maintenance;
The performance deficiency was determined to be more than minor because if left
* Unit 2 Train A Centrifugal Charging Pump Room Cooler Following Maintenance;
uncorrected it would have the potential to lead to a more significant safety concern.
* Unit 2 Train A EDG Room Ventilation Damper Following Replacement; and
Specifically, since the licensees procedures did not contain instructions to properly
* Unit 2 Circuit Card Controlling Auctioneered High Average Temperature Selection. These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable):
inspect the RSH and SXCT, the potential existed for an unacceptable degradation of
the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as
these structures or related components to go undetected affecting essential service
water operability. Inoperable essential service water trains would place the plant at
increased risk for core damage, which would affect the safety of an operating reactor.
The inspectors determined the finding could be evaluated using the Significance
Determination Process (SDP) in accordance with IMC 0609, Significance Determination
Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of
Findings, Table 4a for the Mitigating System Cornerstone. The finding screened as of
very low safety significance (Green) because the finding was a qualification deficiency
confirmed not to result in a loss of operability or functionality. Specifically, the licensee
performed a history review of the surveillance reports and found the documented results
acceptable. A qualitative assessment of the inspections established reasonable
assurance that they did not represent a loss of operability. The inspectors did not have
further concerns.
                                        10                                  Enclosure


written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test
      The inspectors determined that this finding did not represent current licensee
      performance and therefore no cross-cutting aspect was assigned.
      Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
      and Drawings, required, in part, that activities affecting quality shall be prescribed by
      documented instructions, procedures, or drawings, of a type appropriate to the
      circumstances.
      Contrary to the above, as of November 24, 2010, the licensee did not establish RSH and
      SXCT basin surveillance procedural requirements appropriate to the circumstances.
      Specifically, procedure 0BMSR SX-5, Inspection of River Screen House and Essential
      Service Water Cooling Tower Basins (CM-4), the procedure used to inspect these
      structures, was not appropriate for the circumstances. The procedure lacked
      instructions on detecting or recording concrete degradation, erosion, corrosion and
      biological fouling. Without these instructions, the effect of any degradation on system
      operability could not be evaluated. Because this violation was of very low safety
      significance and it was entered into the licensees CAP as IR 1144584, this violation is
      being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.
      (NCV 05000454/2010005-01; 05000455/2010005-01, Inadequate Instructions for the
      Inspection of the River Screen House and Essential Service Water Cooling Tower)
1R11 Licensed Operator Requalification Program (71111.11)
.1    Facility Operating History (71111.11B)
    a. Inspection Scope
      The inspectors reviewed the plants operating history from October 26 through
      October 27, 2010, to identify operating experience that was expected to be addressed
      by the Licensed Operator Requalification Training (LORT) program. The inspector
      verified that the identified operating experience had been addressed by the facility
      licensee in accordance with the stations approved Systems Approach to Training (SAT)
      program to satisfy the requirements of 10 CFR 55.59(c). Documents reviewed are listed
      in the Attachment to this report.
    b. Findings
      No findings of significance were identified.
  .2  Licensee Requalification Examinations
    a. Inspection Scope
      The inspectors performed an inspection of the licensees LORT test/examination
      program for compliance with the stations SAT program which would satisfy the
      requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material
      consisted of two operating tests, each containing two dynamic simulator scenarios and
      six job performance measures (JPMs). The written examinations reviewed consisted of
      two written examinations; each exam contained 30 questions. The inspectors reviewed
      the annual requalification operating test and biennial written examination material to
      evaluate general quality, construction, and difficulty level. The inspectors assessed the
                                              11                                  Enclosure


documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the  
    level of examination material duplication from week-to-week during the current year
equipment met the licensing basis and design requirements.  In addition, the inspectors
    operating test. The examiners assessed the amount of written examination material
reviewed corrective action documents associated with post-maintenance tests to
    duplication from week-to-week for the written examination administered in 2010. The
determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report. This inspection constituted seven post-maintenance testing samples as defined in
    inspectors reviewed the methodology for developing the examinations, including the
IP 71111.19-05. b. Findings
    LORT program 2-year sample plan, probabilistic risk assessment insights, previously
No findings of significance were identified.  
    identified operator performance deficiencies, and plant modifications. Documents
    
    reviewed are listed in the Attachment to this report.
b. Findings
 
    No findings of significance were identified.
19 Enclosure
.3   Licensee Administration of Requalification Examinations
1R22 Surveillance Testing (71111.22) .1 Surveillance Testing
  a. Inspection Scope
  a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural
    The inspectors observed the administration of a requalification operating test to
and TS requirements:
    assess the licensees effectiveness in conducting the test to ensure compliance with
* Unit 2 Local Leakage Rate Test for Primary Containment Purge Supply Isolation
    10 CRF 55.59(c)(4). The inspectors evaluated the performance of two crews in parallel
Valves; and
    with the facility evaluators during two dynamic simulator scenarios and evaluated various
* Unit 2 Train A Containment Spray American Society of Mechanical Engineers (ASME) Surveillance Meeting IST Program Requirements. The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following: 
    licensed crew members concurrently with facility evaluators during the administration of
* did preconditioning occur; 
    several JPMs. The inspectors assessed the facility evaluators ability to determine
* were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
    adequate crew and individual performance using objective, measurable standards. The
* were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
    inspectors observed the training staff personnel administer the operating test, including
* plant equipment calibration was correct, accurate, and properly documented;
    conducting pre-examination briefings, evaluations of operator performance, and
* as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the USAR, procedures, and applicable commitments;
    individual and crew evaluations upon completion of the operating test. The inspectors
* measuring and test equipment calibration was current;
    evaluated the ability of the simulator to support the examinations. A specific evaluation
* test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
    of simulator performance was conducted and documented in the section below titled,
* test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored
    Conformance with Simulator Requirements Specified in 10 CFR 55.46. Documents
where used;
    reviewed are listed in the Attachment to this report.
* test data and results were accurate, complete, within limits, and valid;
  b. Findings
* test equipment was removed after testing;
    No findings of significance were identified.
* where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, ASMEs code, and reference values were consistent with the system design basis;
.4  Examination Security
* where applicable, test results not meeting acceptance criteria were addressed
with an adequate operability evaluation or the system or component was declared inoperable;
* where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
* where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
* prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
* equipment was returned to a position or status required to support the performance of its safety functions; and
20 Enclosure
* all problems identified during the testing were appropriately documented and dispositioned in the CAP.   Documents reviewed are listed in the Attachment to this report. This inspection constituted one inservice testing sample and one containment isolation valve inspection sample as defined in IP 71111.22, Sections -02 and -05. b. Findings
No findings of significance were identified. 2. RADIATION SAFETY Cornerstones:  Occupational and Public Radiation Safety  2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) The inspection activities supplement those documented in Inspection Report 05000454/2010003; 0500455/2010003, and constitute one complete sample as defined in IP 71124.01-05. .1 Contamination and Radioactive Material Control (02.04) a. Inspection Scope
The inspectors selected several sealed sources from the licensee's inventory records and assessed whether the sources were accounted for and verified to be intact. The inspectors evaluated whether any transactions, since the last inspection, involving nationally tracked sources were reported in accordance with 10 CFR 20.2207. b. Findings
No findings of significance were identified. .2 Radiological Hazards Control and Work Coverage (02.05) a. Inspection Scope
The inspectors examined the licensee's physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within spent fuel and other storage
pools.  The inspectors assessed whether appropriate controls (i.e., administrative and
physical controls) were in place to preclude inadvertent removal of these materials from
the pool. b. Findings
No findings of significance were identified.
21 Enclosure
2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06) This inspection constituted a partial sample as defined in IP 71124.06-05. .1 Inspection Planning and Program Reviews (02.01) Event Report and Effluent Report Reviews
  a. Inspection Scope
  a. Inspection Scope
The inspectors reviewed the radiological effluent release reports issued since the last inspection to determine if the reports were submitted as required by the Offsite Dose Calculation Manual/TSs.  The inspectors reviewed anomalous results, unexpected trends, or abnormal releases identified by the licensee for further inspection to determine
    The inspectors observed and reviewed the licensees overall licensed operator
if they were evaluated, were entered in the corrective action program, and were
    requalification examination security program related to examination physical security
adequately resolved. b. Findings
    (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability
No findings of significance were identified. Offsite Dose Calculation Manual and Updated Final Safety Analysis Report Review
    and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.
a. Inspection Scope
    The inspectors also reviewed the facility licensees examination security procedure, any
The inspectors reviewed UFSAR descriptions of the radioactive effluent monitoring
    corrective actions related to past or present examination security problems at the facility,
systems, treatment systems, and effluent flow paths so they can be evaluated during inspection walkdowns.  The inspectors reviewed changes to the Offsite Dose Calculation Manual made by the licensee since the last inspection against the guidance in NUREG-1301 and 0133, and Regulatory Guides 1.109, 1.21 and 4.1.  When differences were identified, the
    and the implementation of security and integrity measures (e.g., security agreements,
inspectors reviewed the technical basis or evaluations of the change during the onsite
    sampling criteria, bank use, and test item repetition) throughout the examination
inspection, to determine whether they were technically justified and maintain effluent releases as-low-as-is-reasonably-achievable. b. Findings
    process. Documents reviewed are listed in the Attachment to this report.
No findings of significance were identified. Procedures, Special Reports, and Other Documents
                                          12                                Enclosure
a. Inspection Scope
The inspectors reviewed copies of licensee and third party (independent) evaluation reports of the effluent monitoring program since the last inspection to gather insights into
the licensee's program and aid in selecting areas for inspection review (smart sampling). b. Findings
No findings of significance were identified. 
22 Enclosure
4. OTHER ACTIVITIES (OA) 4OA1 Performance Indicator Verification (71151) .1 Mitigating Systems Performance Index -
Emergency Alternating Current Power System
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Emergency AC Power System performance indicator (PI) for Unit 1 and Unit 2 for the period from October 1, 2009 through September 30, 2010.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, "Regulatory
Assessment Performance Indicator Guideline," Revision 6, dated October 2009, was
used.  The inspectors reviewed the licensee's operator narrative logs, MSPI derivation
reports, issue reports, event reports and NRC Integrated Inspection Reports for the period of October 1, 2009, through September 30, 2010, to validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk coefficient to determine if
it had changed by more than 25 percent in value since the previous inspection, and if so,
whether the change was in accordance with applicable NEI guidance.  The inspectors
also reviewed the licensee's issue report database to determine if any problems had
been identified with the PI data collected or transmitted for this indicator. Documents  
reviewed are listed in the Attachment to this report. This inspection constituted two MSPI emergency AC power system samples as defined
in IP 71151-05. b. Findings
No findings of significance were identified. .2 Mitigating Systems Performance Index - High Pressure Injection Systems
a. Inspection Scope
The inspectors sampled licensee submittals for the MSPI - High Pressure Injection Systems PI for Unit 1 and Unit 2 for the period from October 1, 2009, through
September 30, 2010.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009, was used.  The
inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI


derivation reports, event reports, and NRC Integrated Inspection Reports for the period of October 1, 2009, through September 30, 2010, to validate the accuracy of the
  b. Findings
submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance.  The inspectors
    No findings of significance were identified.
also reviewed the licensee's issue report database to determine if any problems had
.5  Licensee Training Feedback System
been identified with the PI data collected or transmitted for this indicator.  Documents reviewed are listed in the Attachment to this report. 
23 Enclosure
This inspection constituted two MSPI high pressure injection system samples as defined
in IP 71151-05. b. Findings
No findings of significance were identified. .3 Mitigating Systems Performance Index - Heat Removal System
  a. Inspection Scope
  a. Inspection Scope
The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010.  To determine the accuracy of the PI data reported during those periods, PI definitions and
    The inspectors assessed the methods and effectiveness of the licensees processes for
guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator
    revising and maintaining its LORT Program up to date, including the use of feedback
Guideline," Revision 6, dated October 2009, was used.  The inspectors reviewed the
    from plant events and industry experience information. The inspectors reviewed the
licensee's operator narrative logs, issue reports, event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the period of October 1, 2009, through September 30, 2010, to validate the accuracy of the submittals.  The inspectors
    licensees quality assurance oversight activities, including licensee training department
reviewed the MSPI component risk coefficient to determine if it had changed by more
    self-assessment reports. The inspectors evaluated the licensees ability to assess the
than 25 percent in value since the previous inspection, and if so, whether the change
    effectiveness of its LORT program and their ability to implement appropriate corrective
was in accordance with applicable NEI guidance. The inspectors also reviewed the  
    actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and
licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator.  Documents reviewed are listed in the Attachment to this report. This inspection constituted two MSPI heat removal system samples as defined in
    the licensees SAT program. Documents reviewed are listed in the Attachment to this
IP 71151-05. b. Findings
    report.
No findings of significance were identified. .4 Mitigating Systems Performance Index - Residual Heat Removal System
b. Findings
a. Inspection Scope
    No findings of significance were identified.
The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System PI for Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment
.6   Licensee Remedial Training Program
Performance Indicator Guideline," Revision 6, dated October 2009, was used.  The
inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI
 
derivation reports, event reports, and NRC Integrated Inspection Reports for the period of October 1, 2009, through September 30, 2010, to validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so,
whether the change was in accordance with applicable NEI guidance.  The inspectors
also reviewed the licensee's issue report database to determine if any problems had
been identified with the PI data collected or transmitted for this indicator. Documents
reviewed are listed in the Attachment to this report. 
24 Enclosure
This inspection constituted two MSPI residual heat removal system samples as defined
in IP 71151-05. b. Findings
No findings of significance were identified. .5 Mitigating Systems Performanc
e Index - Cooling Water Systems
a. Inspection Scope
The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010.  To determine the accuracy of the PI data reported during those periods, PI definitions and
guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator
Guideline," Revision 6, dated October 2009, was used.  The inspectors reviewed the
licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports for the period of October 1, 2009 through September 30, 2010, to validate the accuracy of the submittals. The inspectors
reviewed the MSPI component risk coefficient to determine if it had changed by more
than 25 percent in value since the previous inspection, and if so, whether the change
was in accordance with applicable NEI guidance.  The inspectors also reviewed the
licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted two MSPI cooling water system samples as defined in
IP 71151-05. b. Findings
No findings of significance were identified. .6 Reactor Coolant System Specific Activity
  a. Inspection Scope
  a. Inspection Scope
The inspectors sampled licensee submittals for the Reactor Coolant System (RCS) Specific Activity PI for the period from July 2009 through September 2010.  The inspectors used PI definitions and guidance contained in the NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009, to  
    The inspectors assessed the adequacy and effectiveness of the remedial training
determine the accuracy of the PI data reported during those periods. The inspectors  
    conducted since the previous biennial requalification examinations and the training from
reviewed the licensee's RCS chemistry samples, TS requirements, issue reports, event
    the current examination cycle to ensure that they addressed weaknesses in licensed
reports, and NRC Integrated IRs for the per
    operator or crew performance identified during training and plant operations. The
iod of July 2009 through September 2010 to determine if indicator results were accurately reported. Documents reviewed are listed  
    inspectors reviewed remedial training procedures and individual remedial training plans.
in the Attachment to this report This inspection constituted two reactor coolant systems specific activity sample as defined in IP 71151-05.
    This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to
25 Enclosure
    the licensees SAT program. Documents reviewed are listed in the Attachment to this
    report.
  b. Findings
  b. Findings
No findings of significance were identified. .7 Occupational Exposure Control Effectiveness
    No findings of significance were identified.
.7   Conformance with Operator License Conditions
  a. Inspection Scope
  a. Inspection Scope
The inspectors sampled licensee submittals for the Occupational Radiological Occurrences PI for the period of July 2009 through September 2010.  The inspectors used PI definitions and guidance contained in the NEI 99-02, "Regulatory Assessment
    The inspectors reviewed the facility and individual operator licensees' conformance with
Performance Indicator Guideline," Revision 6, dated October 2009, to determine the  
    the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's
accuracy of the PI data reported during those periods. The inspectors reviewed  
    program for maintaining active operator licenses and to assess compliance with
electronic dosimetry dose rate and accumulated dose alarm and dose reports and the dose assignments for any intakes that occurred for selected dates between July 2009 and September 2010 to determine if indicator results were accurately reported.  The
    10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the
inspectors also conducted walk downs of numerous locked high and very high radiation
    process for tracking on-shift hours for licensed operators and which control room
area entrances to determine the adequacy of the controls in place for these areas.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one occupational radiological occurrences sample as defined
    positions were granted watch-standing credit for maintaining active operator licenses.
in IP 71151-05. b. Findings
    The inspectors reviewed the facility licensee's LORT program to assess compliance with
No findings of significance were identified. .8 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
    the requalification program requirements as described by 10 CFR 55.59(c). Additionally,
Radiological Effluent Occurrences
    medical records for 10 licensed operators were reviewed for compliance with
a. Inspection Scope
                                          13                                  Enclosure
The inspectors sampled licensee submittals for the Radiological Effluent Technical Specification (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent
 
Occurrences performance indicator for the period of July 2009 through September 2010.
    10 CFR 55.21 and 55.53(i). Documents reviewed are listed in the Attachment to this
The inspectors used PI definitions and guidance contained in the NEI 99-02, "Regulatory
    report.
Assessment Performance Indicator Guideline," Revision 6, dated October 2009, to determine the accuracy of the PI data reported during those periods. The inspectors reviewed the licensee's issue report database and selected individual reports generated
since this indicator was last reviewed to identify any potential occurrences such as  
unmonitored, uncontrolled, or improperly calculated effluent releases that may have
impacted offsite dose.  The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates from July 2009 through September 2010 to determine if indicator results were accurately reported.  The
inspectors also reviewed the licensee's methods for quantifying gaseous and liquid
effluents and determining effluent dose. Documents reviewed are listed in the Attachment to this report. This inspection constituted one RETS/ODCM radiological effluent occurrences sample
as defined in IP 71151-05. 
26 Enclosure
  b. Findings
  b. Findings
No findings of significance were identified. 4OA2 Identification and Resolution of Problems (71152) Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
    No findings of significance were identified.
Physical Protection .1 Routine Review of Items Entered into the Corrective Action Program
.8  Conformance with Simulator Requirements Specified in 10 CFR 55.46
  a. Inspection Scope
  a. Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's CAP at
    The inspectors assessed the adequacy of the licensees simulation facility (simulator) for
an appropriate threshold, that adequate attention was being given to timely corrective
    use in operator licensing examinations and for satisfying experience requirements as
actions, and that adverse trends were identified and addressed. Attributes reviewed  
    prescribed in 10 CFR 55.46, Simulation Facilities. The inspectors also reviewed a
included:  the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root
    sample of simulator performance test records (i.e., transient tests, malfunction tests,
causes, extent-of-condition reviews, and previous occurrences reviews were proper and
    steady state tests, and core performance tests), simulator discrepancies, and the
adequate; and that the classification, prioritization, focus, and timeliness of corrective
    process for ensuring continued assurance of simulator fidelity in accordance with
actions were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensee's CAP as a result of the inspectors' observations are included in the attached List of Documents Reviewed. These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an
    10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to
integral part of the inspections performed during the quarter and documented in Section 1 of this report. b. Findings
    ensure that simulator fidelity was maintained. Open simulator discrepancies were
No findings of significance were identified. .2 Daily Corrective Action Program Reviews
    reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator
a. Inspection Scope
    actions as well as on nuclear and thermal hydraulic operating characteristics. The
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP.  This review was accomplished through inspection of the station's daily condition report packages. These daily reviews were performed by procedure as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
    inspectors conducted interviews with members of the licensees simulator staff about the
27 Enclosure
    configuration control process and completed the IP 71111.11, Appendix C, checklist to
    evaluate whether or not the licensees plant-referenced simulator was operating
    adequately as required by 10 CFR 55.46(c) and (d). Documents reviewed are listed in
    the Attachment to this report.
  b. Findings
  b. Findings
No findings of significance were identified. .3 Semi Annual Trend Review
    No findings of significance were identified.
a. Inspection Scope
.9  Resident Inspector Quarterly Review (71111.11Q)
The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue.  The inspectors' review was focused on repetitive equipment issues, but also considered the
results of daily inspector CAP item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results.  The inspectors'
review nominally considered the 6 month period of June 1, 2010, through November 30, 2010, although some examples expanded beyond those dates where the scope of the trend warranted. The review also included issues documented outside the normal CAP; including major equipment problem lists, repetitive and/or rework maintenance lists, departmental
problem/challenges lists, system health reports, quality assurance audit/surveillance
reports, self assessment reports, and Maintenance Rule assessments. The inspectors
compared and contrasted their results with the results contained in the licensee's
CAP trending reports.  Corrective actions associated with a sample of the issues
identified in the licensee's trending reports were reviewed for adequacy. This review constituted a single semi-annual trend inspection sample as defined in
IP 71152-05. b. Findings
No findings of significance were identified. .4 Annual Sample:  Review of Operator Workarounds
  a. Inspection Scope
  a. Inspection Scope
The inspectors evaluated the licensee's implementation of their process used to identify, document, track, and resolve operational challenges.  Inspection activities included, but
    On October 26 and October 27, 2010, the inspectors observed two crews of licensed
were not limited to, a review of the cumulative effects of the Operator Workarounds (OWAs) on system availability and the potential for improper operation of the system, for potential impacts on multiple systems, and on the ability of operators to respond to plant transients or accidents. The inspectors performed a review of the cumulative effects of OWAs.  The documents listed in the Attachment were reviewed to accomplish the objectives of the inspection
    operators in the plants simulator during licensed operator requalification examinations to
procedure.  The inspectors reviewed both current and historical operational challenge
    verify that operator performance was adequate, evaluators were identifying and
records to determine whether the licensee was identifying operator challenges at an
    documenting crew performance problems, and training was being conducted in
appropriate threshold, had entered them into their CAP, and proposed or implemented appropriate and timely corrective actions which addressed each issue.  Reviews were conducted to determine if any operator challenge could increase the possibility of an initiating event, if the challenge was contrary to training, required a change from long-standing operational practices, or created the potential for inappropriate 
    accordance with licensee procedures. The inspectors evaluated the following areas:
28 Enclosure
    *        licensed operator performance;
compensatory actions.  Additionally, all temporary modifications were reviewed to identify any potential effect on the functionality of Mitigating Systems, impaired access to
    *        crews clarity and formality of communications;
equipment, or required equipment uses for which the equipment was not designed.  Daily plant and equipment status logs, degraded instrument logs, and operator aids or tools being used to compensate for material deficiencies were also assessed to identify any potential sources of unidentified operator workarounds. This review constituted one operator workaround annual inspection sample as defined in
    *        ability to take timely actions in the conservative direction;
IP 71152-05. b. Findings
    *        prioritization, interpretation, and verification of annunciator alarms;
No findings of significance were identified. 4OA3 Followup of Events and Notices of Enforcement Discretion (71153) .1 (Closed) Licensee Event Report 05000455/2010-001-00
    *        correct use and implementation of abnormal and emergency procedures;
:  Reactor Protection and Auxiliary Feedwater Actuation Signals from Low Steam Generator (S/G) Level Due to Inadequate Surveillance Testing On April 19, 2010, Unit 2 was in the process of shutting down and cooling down in order to enter a planned refuelling outage.  At 5:03 am with the unit in Mode 4, Hot Shutdown, a feedwater isolation valve (FWIV) surveillance was in progress and the 2D S/G secondary side water level lowered to the low S/G water level setpoint, which resulted in  
    *        control board manipulations;
a valid FWIV actuation.  All equipment actuated properly and due to the plant condition, the control rods were already fully inserted with the reactor trip breakers open.  The licensee's apparent cause evaluation determined that the operators had received Just-In-Time training immediately prior to the refuelling outage. However, inadequate
    *        oversight and direction from supervisors; and
oversight combined with an inadequate procedure had resulted in inadequate control of the surveillance test activity.  The licensee determined that the surveillance procedure did not allow for S/G levels to be recovered between the testing of the two trains,
    *        ability to identify and implement appropriate TS actions and Emergency Plan
performance of the test during the outage was not performed at the optimum time based
            actions and notifications.
on plant parameters, and no pre-job briefing was performed the night of the test.  The
                                              14                                  Enclosure
licensee had determined that while the test was performed during a time in the outage that it was usually performed that it had been performed when the RCS was hotter than it had been before, which resulted in the S/G water level steaming off at a faster rate
than previously experienced. The inspectors reviewed the Licensee Event Report (LER), licensee procedures, and performed interviews of selected licensee personnel.  The inspectors agreed with the
licensee's apparent cause evaluation conclusion regarding the three causes of the FWIV
actuation.  The inspectors reviewed the licensee's corrective actions and verified that the
corrective actions addressed the causes and were implemented.  Corrective actions included revising the FWIV surveillance procedure, strengthening pre-job briefs, and reinforcing the roles and responsibilities of key outage operations positions. Although this issue was corrected, it constituted a performance deficiency and a minor violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and
Drawings."  However, it is not subject to enforcement action in accordance with
Section 2.3.1 of the Enforcement Policy.  Because the performance deficiency was not 
29 Enclosure  
more than minor and not a finding per IMC 0612, Appendix B, "Issue Screening," a cross-cutting aspect was not assigned to this violation. 


This event follow-up review constituted one sample as defined in IP 71153-05.  
      The crews performance in these areas was compared to pre-established operator action
4OA5 Other Activities
      expectations and successful critical task completion requirements. Documents reviewed
.1 Review of Institute of Nuclear Power Operations Report
      are listed in the Attachment to this report.
The inspectors reviewed the Institute of Nuclear Power Operations July 2010 Evaluation Report, Byron Station, dated December 10, 2010. .2 Operation of an Independent Spent Fuel Storage Installation at Operating Plants
      This inspection constituted one quarterly licensed operator requalification program
(60855.1) a. Inspection Scope
      sample as defined in IP 71111.11-05.
The inspectors observed and evaluated the licensee's loading operations of the first and second multi-purpose canisters (MPC) during the licensee's initial spent fuel loading
    b. Findings
campaign to verify compliance with the Cert
      No findings of significance were identified.
ificate of Compliance, TS, NRC Regulations, and associated procedures. The inspectors observed heavy loads movements inside
1R12 Maintenance Effectiveness (71111.12)
the Fuel Handling Building (FHB) including: lifting of the transfer cask (HI-TRAC) into the spent fuel pool, lifting of the HI-TRAC from the spent fuel pool to the decontamination stand, and transfer of the MPC from the HI-TRAC to the storage cask (HI-STORM) while
.1    Routine Quarterly Evaluations (71111.12Q)
the casks are stacked on one another in a laterally restrained configuration. The  
    a. Inspection Scope
inspectors observed loading of spent fuel assemblies from the spent fuel pool into the  
      The inspectors evaluated degraded performance issues involving the following
MPC.  The inspectors observed MPC processing operations including:  decontamination and surveying, canister welding, non-destructive weld examinations, hydrostatic testing, canister draining, vacuum drying, and helium backfilling. The inspectors observed heavy
      risk-significant systems:
loads operations outside of the FHB including: transfer of the HI-STORM from inside of
      *        Failure of Unit 2 Train A EDG Upper Lube Oil Cooler Fixed End Flange
the FHB to outside of the FHB on a low profile transporter, and transfer of the
                Connection.
HI-STORM to the Independent Spent Fuel Storage Installation (ISFSI) pad using a
      The inspectors reviewed events such as where ineffective equipment maintenance had
vertical cask transporter.
      resulted in valid or invalid automatic actuations of engineered safeguards systems and
During performance of the activities, the inspectors evaluated the licensee staff's
      independently verified the licensee's actions to address system performance or condition
familiarity with procedures, supervisory oversight, and communication and coordination
      problems in terms of the following:
between the different groups involved. The inspectors reviewed loading procedures and
      *        implementing appropriate work practices;
evaluated the licensee's adherence to these procedures.  The inspectors also observed the licensee's process to verify that the contamination and radiation levels from the transfer cask and storage cask were below the regulatory and TS limits.  The inspectors
      *        identifying and addressing common cause failures;
attended various pre-job briefs to assess the licensee's ability to identify critical steps of  
      *        scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
the evolution, potential failure scenarios, and tools to prevent errors. 
      *        characterizing system reliability issues for performance;
      *        charging unavailability for performance;
      *        trending key parameters for condition monitoring;
      *        ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
      *        verifying appropriate performance criteria for structures, systems, and
                components (SSCs)/functions classified as (a)(2) or appropriate and adequate
                goals and corrective actions for systems classified as (a)(1).
      The inspectors assessed performance issues with respect to the reliability, availability,
      and condition monitoring of the system. In addition, the inspectors verified maintenance
      effectiveness issues were entered into the CAP with the appropriate significance
      characterization. Documents reviewed are listed in the Attachment to this report.
      This inspection constituted one quarterly maintenance effectiveness samples as defined
      in IP 71111.12-05.
    b. Findings
      No findings of significance were documented in this inspection report. Additional follow-
      up and regulatory conclusions are the subject of NRC IR 05000455/2011011.
                                              15                                  Enclosure


  The inspectors reviewed issue reports and the associated follow-up actions that were generated during the loading campaign as well as 10 CFR 72.48 screenings.  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  .1  Maintenance Risk Assessments and Emergent Work Control
  a. Inspection Scope
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
      maintenance and emergent work activities affecting risk-significant and safety-related
      equipment listed below to verify that the appropriate risk assessments were performed
      prior to removing equipment for work:
      *        Work Activities during the Week of November 8 Focusing on Unit 2 Train A SX
              Outage; and
      *        Work Activities during the Week of November 29 for Unit 1 Emergent Direct
              Current (DC) Bus 112 Battery Cell Replacement and Planned Unit 2 Safety
              Injection Pump work window.
      These activities were selected based on their potential risk significance relative to the
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
      and complete. When emergent work was performed, the inspectors verified that the
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
      of maintenance work, discussed the results of the assessment with the licensee's
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
      walked down portions of redundant safety systems, when applicable, to verify risk
      analysis assumptions were valid and applicable requirements were met.
      These maintenance risk assessments and emergent work control activities constituted
      two samples as defined in IP 71111.13-05.
  b. Findings
      No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
.1  Operability Evaluations
  a. Inspection Scope
      The inspectors reviewed the following issues:
      *        Unit 2 Train A Pressurizer Safety Valve Due to Identified but Unexpected Leakby;
      *        Unit 2 Train A SX Foreign Material Discovered within the Lube Oil Pump; and
      *        Unit 1 Train B Auxiliary Feedwater Pump Oil Cooler Piping Configuration Error.
      The inspectors selected these potential operability issues based on the risk significance
      of the associated components and systems. The inspectors evaluated the technical
      adequacy of the evaluations to ensure that TS operability was properly justified and the
      subject component or system remained available such that no unrecognized increase in
                                              16                                  Enclosure


      risk occurred. The inspectors compared the operability and design criteria in the
On Saturday, August 28, 2010, the licensee's first MPC containing spent nuclear fuel
      appropriate sections of the TS and USAR to the licensees evaluations to determine
was left unmonitored during processing operations at the end-of-shift operations.  The
      whether the components or systems were operable. Where compensatory measures
MPC had been undergoing vacuum drying throughout the day and at the end of shift was left under vacuum. While the canister was under vacuum, cooling of the fuel was significantly reduced, and subsequently fuel temperatures were elevated. The licensee's 
      were required to maintain operability, the inspectors determined whether the measures
30 Enclosure
      in place would function as intended and were properly controlled. The inspectors
safety analysis for the spent fuel cask system required that the MPC shell temperature be maintained below 125 degrees Fahrenheit (°F) while the MPC is under vacuum. A
      determined, where appropriate, compliance with bounding limitations associated with the
MPC shell temperature of 125°F corresponds to a design basis limit of 1040°F for fuel cladding temperature as discussed in the Holtec HI-STORM 100 FSAR, Revision 5Cooling of the water contained within the HI-TRAC annulus, the area between the MPC
      evaluations. Additionally, the inspectors reviewed a sampling of corrective action
and the HI-TRAC, is provided by a chiller unit when required.  For the fuel selected,  
      documents to verify that the licensee was identifying and correcting any deficiencies
annulus cooling would be required to maintain the MPC shell temperature below 125
      associated with operability evaluations. Documents reviewed are listed in the
o F.  Prior to the end of shift on August 28, 2010, the inspectors asked the licensee what
      Attachment to this report.
plans were in place for monitoring the MPC overnight. The inspectors were informed that various options were being considered for monitoring the MPC overnight and that a final decision on the exact method of monitoring and specific staffing had not been
      This operability inspection constituted three samples as defined in IP 71111.15-05.
determined. Later that evening, the licensee discussed the importance of the chiller with  
  b. Findings
technical experts and determined that, due to the heat loads selected for this canister,
      No findings of significance were identified.
heat rates were not high enough to exceed fuel temperature limits even in the event of a chiller shut off. Therefore, the licensee concluded that no monitoring was necessary overnight. No specific analysis was performed to support this determination.  
1R18 Plant Modifications (71111.18)
  .1  Temporary Plant Modifications
  a. Inspection Scope
      The inspectors reviewed the following temporary modifications:
      *      Unit 2 Temporarily Disconnect Both Sudden Pressure Relays for Main Power
              Transformer 2MP01E due to Ground Associated with Relay 63-1; and
      *      Unit 1 Battery Bank 112 Installation of Jumper for Degraded Cell.
      The inspectors compared the temporary configuration changes and associated
      10 CFR 50.59 screening and evaluation information against the design basis, the
      UFSAR, and the TS, as applicable, to verify that the modification did not affect the
      operability or availability of the affected system(s). The inspectors also compared the
      licensees information to operating experience information to ensure that lessons learned
      from other utilities had been incorporated into the licensees decision to implement the
      temporary modification. The inspectors, as applicable, performed field verifications to
      ensure that the modifications were installed as directed; the modifications operated as
      expected; modification testing adequately demonstrated continued system operability,
      availability, and reliability; and that operation of the modifications did not impact the
      operability of any interfacing systems. Lastly, the inspectors discussed the temporary
      modification with operations, engineering, and training personnel to ensure that the
      individuals were aware of how extended operation with the temporary modification in
      place could impact overall plant performance. Documents reviewed are listed in the
      Attachment to this report.
      This inspection constituted two temporary modification samples as defined in
      IP 71111.18-05.
  b. Findings
      No findings of significance were identified.
                                                17                                Enclosure


   
1R19 Post Maintenance Testing (71111.19)
On the morning of August 29, 2010, the licensee identified that the chiller had
  .1  Post Maintenance Testing
unexpectedly shut off overnight; however, the licensee failed to recognize that the annulus water temperature corresponded to a safety limit for fuel cladding temperature as discussed in the FSAR.  A back-up chiller was placed in service promptly; however,
  a. Inspection Scope
the licensee did not recognize the importance of determining the current water
      The inspectors reviewed the following post-maintenance activities to verify that
temperature to ensure that no safety limits were exceeded. The inspectors notified the  
      procedures and test activities were adequate to ensure system operability and
licensee of the design basis annulus water temperature limit of 125
      functional capability:
o F, which was specified in the FSAR.  The inspectors estimated that the 125
      *      Unit 1 Train A Chemical Volume Control Pump Room Cooling Fan Following
oF limit was likely exceeded by several degrees. 
              Motor Replacement;
      *      Unit 1 Train B EDG Following Planned Maintenance Work Window;
The licensee began a prompt evaluation to determine if any fuel cladding safety limits
      *      Unit 1 Battery Bank 112 Installation of Jumper for Degraded Cell;
were exceeded. Working with the licens
      *      Unit 2 Train B Auxiliary Feedwater Pump Following Maintenance;
ee's vendor, Holtec, the prompt evaluation concluded that no fuel cladding safety limits were exceeded. 
      *      Unit 2 Train A Centrifugal Charging Pump Room Cooler Following Maintenance;
In response to the circumstances of August 28 and 29, 2010, the NRC increased the oversight of the ISFSI project at the Byron Station and began a reactive inspection on
      *      Unit 2 Train A EDG Room Ventilation Damper Following Replacement; and
September 1, 2010. The results of this reactive inspection are documented in NRC
      *      Unit 2 Circuit Card Controlling Auctioneered High Average Temperature
IR Nos. 05000454/2010007; 05000455/2010007; and 07200068/2010002.  
              Selection.
      These activities were selected based upon the structure, system, or component's ability
      to impact risk. The inspectors evaluated these activities for the following (as applicable):
      the effect of testing on the plant had been adequately addressed; testing was adequate
      for the maintenance performed; acceptance criteria were clear and demonstrated
      operational readiness; test instrumentation was appropriate; tests were performed as
      written in accordance with properly reviewed and approved procedures; equipment was
      returned to its operational status following testing (temporary modifications or jumpers
      required for test performance were properly removed after test completion); and test
      documentation was properly evaluated. The inspectors evaluated the activities against
      TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
      NRC generic communications to ensure that the test results adequately ensured that the
      equipment met the licensing basis and design requirements. In addition, the inspectors
      reviewed corrective action documents associated with post-maintenance tests to
      determine whether the licensee was identifying problems and entering them in the CAP
      and that the problems were being corrected commensurate with their importance to
      safety. Documents reviewed are listed in the Attachment to this report.
      This inspection constituted seven post-maintenance testing samples as defined in
      IP 71111.19-05.
  b. Findings
      No findings of significance were identified.
                                              18                                Enclosure


  Following completion of the reactive inspection the inspectors reviewed the licensee's corrective actions that had been completed and subsequent procedure changes.  The
1R22 Surveillance Testing (71111.22)
ISFSI inspectors remained onsite for the licensee's second MPC loading operations. 
  .1  Surveillance Testing
Following the second MPC loading, ISFSI inspectors monitored loading operations from
  a. Inspection Scope
the regional office.
      The inspectors reviewed the test results for the following activities to determine whether
b. Findings
      risk-significant systems and equipment were capable of performing their intended safety
(1) Inadequate Procedures for Implementing Final Safety Analysis Report Required Annulus
      function and to verify testing was conducted in accordance with applicable procedural
Cooling  Introduction:  The inspectors identified a Severity Level IV NCV of very low safety significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings."  Specifically, 
      and TS requirements:
31 Enclosure
      *      Unit 2 Local Leakage Rate Test for Primary Containment Purge Supply Isolation
the licensee failed to have procedures in place to ensure that the design basis peak fuel cladding temperature limit would not be exceeded during canister loading operations.
              Valves; and
  Description:  The licensee revised their ISFSI loading procedures following the circumstances of August 28 and 29.  During review of the revised procedures, the  
      *      Unit 2 Train A Containment Spray American Society of Mechanical Engineers
inspectors identified three examples where the licensee failed to meet the requirements in 10 CFR 72.150, "Instructions, Procedures, and Drawings."
              (ASME) Surveillance Meeting IST Program Requirements.
1. Byron Fuel Handling Procedure BFP FH-71, "MPC Processing", Revision 8, provides guidance for the licensee to complete MPC processing operations. 
      The inspectors observed in-plant activities and reviewed procedures and associated
The Holtec FSAR, Revision 5, Chapter 4, discussed how the fuel cladding
      records to determine the following:
temperature limits and associated hoop stress calculation requirements were
      *      did preconditioning occur;
consistent with the guidance in Spent Fuel Storage and Transportation (SFST)
      *      were the effects of the testing adequately addressed by control room personnel
              or engineers prior to the commencement of the testing;
      *      were acceptance criteria clearly stated, demonstrated operational readiness, and
              consistent with the system design basis;
      *      plant equipment calibration was correct, accurate, and properly documented;
      *      as-left setpoints were within required ranges; and the calibration frequency were
              in accordance with TSs, the USAR, procedures, and applicable commitments;
      *      measuring and test equipment calibration was current;
      *      test equipment was used within the required range and accuracy; applicable
              prerequisites described in the test procedures were satisfied;
      *      test frequencies met TS requirements to demonstrate operability and reliability;
              tests were performed in accordance with the test procedures and other
              applicable procedures; jumpers and lifted leads were controlled and restored
              where used;
      *      test data and results were accurate, complete, within limits, and valid;
      *      test equipment was removed after testing;
      *      where applicable for inservice testing activities, testing was performed in
              accordance with the applicable version of Section XI, ASMEs code, and
              reference values were consistent with the system design basis;
      *      where applicable, test results not meeting acceptance criteria were addressed
              with an adequate operability evaluation or the system or component was
              declared inoperable;
      *      where applicable for safety-related instrument control surveillance tests,
              reference setting data were accurately incorporated in the test procedure;
      *      where applicable, actual conditions encountering high resistance electrical
              contacts were such that the intended safety function could still be accomplished;
      *      prior procedure changes had not provided an opportunity to identify problems
              encountered during the performance of the surveillance or calibration test;
      *      equipment was returned to a position or status required to support the
              performance of its safety functions; and
                                            19                                  Enclosure


Interim Staff Guidance (ISG) - 11 during vac
      *      all problems identified during the testing were appropriately documented and
uum drying operations. Specifically, the Holtec FSAR, Revision 5, Section 4.5.1.1.4.1, "Vacuum Drying" states, in part:
              dispositioned in the CAP.
  "The initial loading of Spent Nuclear Fuel in the MPC requires that the water within the MPC be drained and replaced with helium. For MPCs containing moderate burn-up fuel assemblies only, this operation may be carried out using the conventional vacuum drying approach. In this method, removal of the last
      Documents reviewed are listed in the Attachment to this report.
traces of residual moisture from the MPC cavity is accomplished by evacuating
      This inspection constituted one inservice testing sample and one containment isolation
the MPC for a short time after draining the MPC."
      valve inspection sample as defined in IP 71111.22, Sections -02 and -05.
  b. Findings
      No findings of significance were identified.
2.   RADIATION SAFETY
      Cornerstones: Occupational and Public Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
      The inspection activities supplement those documented in Inspection
      Report 05000454/2010003; 0500455/2010003, and constitute one complete
      sample as defined in IP 71124.01-05.
  .1  Contamination and Radioactive Material Control (02.04)
  a. Inspection Scope
      The inspectors selected several sealed sources from the licensees inventory records
      and assessed whether the sources were accounted for and verified to be intact.
      The inspectors evaluated whether any transactions, since the last inspection, involving
      nationally tracked sources were reported in accordance with 10 CFR 20.2207.
  b. Findings
      No findings of significance were identified.
  .2  Radiological Hazards Control and Work Coverage (02.05)
  a. Inspection Scope
      The inspectors examined the licensees physical and programmatic controls for highly
      activated or contaminated materials (nonfuel) stored within spent fuel and other storage
      pools. The inspectors assessed whether appropriate controls (i.e., administrative and
      physical controls) were in place to preclude inadvertent removal of these materials from
      the pool.
  b. Findings
      No findings of significance were identified.
                                            20                                Enclosure


"For any decay heat load in an MPC-32, vacuum drying of the MPC is performed with the annular gap between the MPC and the HI-TRAC continuously flushed
2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
with water. The water movement in this annular gap will maintain the MPC shell
      This inspection constituted a partial sample as defined in IP 71124.06-05.
temperature at about the temperature of flowing water. Thus, the thermal
.1  Inspection Planning and Program Reviews (02.01)
analysis of the MPC during vacuum drying for these conditions is performed with
      Event Report and Effluent Report Reviews
cooling of the MPC shell with water at a bounding maximum temperature of
  a. Inspection Scope
125 o F.
      The inspectors reviewed the radiological effluent release reports issued since the last
"To avoid excessive conservatism in the computed FLUENT
      inspection to determine if the reports were submitted as required by the Offsite Dose
solution, partial recognition for higher axial heat dissipation is adopted in the peak cladding
      Calculation Manual/TSs. The inspectors reviewed anomalous results, unexpected
calculations. The boundary conditions applied to this evaluation are:  ii.  The entire outer surface of the MPC shell is postulated to be at a bounding maximum
      trends, or abnormal releases identified by the licensee for further inspection to determine
temperature of 125°F.
      if they were evaluated, were entered in the corrective action program, and were
As described in the Holtec FSAR, the intent of flushing water through the annulus
      adequately resolved.
region between the HI-TRAC and the MPC is to maintain the surface of the MPC shell below 125 °F.  The Holtec FSAR states that if MPC shell temperature remains below 125 °F, the peak fuel cladding temperatures, for moderate burn-up fuel, during
  b. Findings
short-term vacuum drying operations, in an MPC with design basis maximum heat
      No findings of significance were identified.
loads, are calculated to be less than the SFST ISG-11 safety limit of 1058ºF.  
      Offsite Dose Calculation Manual and Updated Final Safety Analysis Report Review
  a. Inspection Scope
      The inspectors reviewed UFSAR descriptions of the radioactive effluent monitoring
      systems, treatment systems, and effluent flow paths so they can be evaluated during
      inspection walkdowns.
      The inspectors reviewed changes to the Offsite Dose Calculation Manual made by the
      licensee since the last inspection against the guidance in NUREG-1301 and 0133, and
      Regulatory Guides 1.109, 1.21 and 4.1. When differences were identified, the
      inspectors reviewed the technical basis or evaluations of the change during the onsite
      inspection, to determine whether they were technically justified and maintain effluent
      releases as-low-as-is-reasonably-achievable.
  b. Findings
      No findings of significance were identified.
      Procedures, Special Reports, and Other Documents
  a. Inspection Scope
      The inspectors reviewed copies of licensee and third party (independent) evaluation
      reports of the effluent monitoring program since the last inspection to gather insights into
      the licensees program and aid in selecting areas for inspection review (smart sampling).
  b. Findings
      No findings of significance were identified.
                                            21                                Enclosure


   
4.    OTHER ACTIVITIES (OA)
During vacuum drying operations at the Byron Station, the seal that maintains water inside the annulus region is removed and allowed to flood several inches over the top of the MPC.  The licensee's procedures required the annulus water to be cooled
4OA1 Performance Indicator Verification (71151)
  .1 Mitigating Systems Performance Index - Emergency Alternating Current Power System
  a. Inspection Scope
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
      Index (MSPI) - Emergency AC Power System performance indicator (PI) for Unit 1 and
      Unit 2 for the period from October 1, 2009 through September 30, 2010. To determine
      the accuracy of the PI data reported during those periods, PI definitions and guidance
      contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory
      Assessment Performance Indicator Guideline, Revision 6, dated October 2009, was
      used. The inspectors reviewed the licensees operator narrative logs, MSPI derivation
      reports, issue reports, event reports and NRC Integrated Inspection Reports for the
      period of October 1, 2009, through September 30, 2010, to validate the accuracy of the
      submittals. The inspectors reviewed the MSPI component risk coefficient to determine if
      it had changed by more than 25 percent in value since the previous inspection, and if so,
      whether the change was in accordance with applicable NEI guidance. The inspectors
      also reviewed the licensees issue report database to determine if any problems had
      been identified with the PI data collected or transmitted for this indicator. Documents
      reviewed are listed in the Attachment to this report.
      This inspection constituted two MSPI emergency AC power system samples as defined
      in IP 71151-05.
  b. Findings
      No findings of significance were identified.
  .2  Mitigating Systems Performance Index - High Pressure Injection Systems
  a. Inspection Scope
      The inspectors sampled licensee submittals for the MSPI - High Pressure Injection
      Systems PI for Unit 1 and Unit 2 for the period from October 1, 2009, through
      September 30, 2010. To determine the accuracy of the PI data reported during those
      periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment
      Performance Indicator Guideline, Revision 6, dated October 2009, was used. The
      inspectors reviewed the licensees operator narrative logs, issue reports, MSPI
      derivation reports, event reports, and NRC Integrated Inspection Reports for the period
      of October 1, 2009, through September 30, 2010, to validate the accuracy of the
      submittals. The inspectors reviewed the MSPI component risk coefficient to determine if
      it had changed by more than 25 percent in value since the previous inspection, and if so,
      whether the change was in accordance with applicable NEI guidance. The inspectors
      also reviewed the licensees issue report database to determine if any problems had
      been identified with the PI data collected or transmitted for this indicator. Documents
      reviewed are listed in the Attachment to this report.
                                            22                                  Enclosure


with a submersible pump, heat exchanger, and chillerThe submersible pump took a suction of water above the MPC lid and discharged water on the other side of the 
    This inspection constituted two MSPI high pressure injection system samples as defined
32 Enclosure
    in IP 71151-05.
  MPC lid. Temperature measurements were recorded near the suction and discharge locations. The licensee failed to have an analysis demonstrating that temperatures
  b. Findings
measured at the top of the MPC where
    No findings of significance were identified.
water was being continuously flushed by a submersible pump was indicative of canister shell temperatures on the side of the MPC where water was not being continuously flushed. The licensee failed to  
.3  Mitigating Systems Performance Index - Heat Removal System
configure the intake and discharge of the submersible pump to ensure that all
  a. Inspection Scope
regions of the MPC were continuously flushed with water and subsequently failed to  
    The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for
ensure that temperature measurements taken were indicative of the highest shell
    Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010. To
temperatures present.  The licensee entered these issues into its CAP (IR 1131564) and initiated actions to evaluate the condition. Following the event, the licensee contacted the cask vendor, Holtec, and completed an analysis to show that peak fuel
    determine the accuracy of the PI data reported during those periods, PI definitions and
cladding temperature limits were not exceeded. The licensee revised the
    guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator
configuration of the pump such that the pump intake was at the top of the annulus
    Guideline, Revision 6, dated October 2009, was used. The inspectors reviewed the
and the pump discharge was through the annulus drain line near the bottom of the annulus.  2. The BFP FH-71, "MPC Processing", Revision 8, provides guidance for the licensee to complete MPC processing operations. 
    licensees operator narrative logs, issue reports, event reports, MSPI derivation reports,
As previously discussed in 4OA5.2.b.1.1, the annulus between the MPC and the HI-TRAC is required to be continuously flushed with water to ensure that the MPC
    and NRC Integrated Inspection Reports for the period of October 1, 2009, through
shell temperature is maintained below the design basis limit of 125
    September 30, 2010, to validate the accuracy of the submittals. The inspectors
oF in order to maintain fuel cladding peak temperatures under design limits as described in the
    reviewed the MSPI component risk coefficient to determine if it had changed by more
    than 25 percent in value since the previous inspection, and if so, whether the change
    was in accordance with applicable NEI guidance. The inspectors also reviewed the
    licensees issue report database to determine if any problems had been identified with
    the PI data collected or transmitted for this indicator. Documents reviewed are listed in
    the Attachment to this report.
    This inspection constituted two MSPI heat removal system samples as defined in
    IP 71151-05.
b. Findings
    No findings of significance were identified.
.4  Mitigating Systems Performance Index - Residual Heat Removal System
  a. Inspection Scope
    The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal
    System PI for Unit 1 and Unit 2, for the period from October 1, 2009, through
    September 30, 2010. To determine the accuracy of the PI data reported during those
    periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment
    Performance Indicator Guideline, Revision 6, dated October 2009, was used. The
    inspectors reviewed the licensees operator narrative logs, issue reports, MSPI
    derivation reports, event reports, and NRC Integrated Inspection Reports for the period
    of October 1, 2009, through September 30, 2010, to validate the accuracy of the
    submittals. The inspectors reviewed the MSPI component risk coefficient to determine if
    it had changed by more than 25 percent in value since the previous inspection, and if so,
    whether the change was in accordance with applicable NEI guidance. The inspectors
    also reviewed the licensees issue report database to determine if any problems had
    been identified with the PI data collected or transmitted for this indicator. Documents
    reviewed are listed in the Attachment to this report.
                                          23                                  Enclosure


Holtec FSAR, Revision 5.  
    This inspection constituted two MSPI residual heat removal system samples as defined
    in IP 71151-05.
  b. Findings
    No findings of significance were identified.
.5  Mitigating Systems Performance Index - Cooling Water Systems
  a. Inspection Scope
    The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI
    Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010. To
    determine the accuracy of the PI data reported during those periods, PI definitions and
    guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator
    Guideline, Revision 6, dated October 2009, was used. The inspectors reviewed the
    licensees operator narrative logs, issue reports, MSPI derivation reports, event reports,
    and NRC Integrated Inspection Reports for the period of October 1, 2009 through
    September 30, 2010, to validate the accuracy of the submittals. The inspectors
    reviewed the MSPI component risk coefficient to determine if it had changed by more
    than 25 percent in value since the previous inspection, and if so, whether the change
    was in accordance with applicable NEI guidance. The inspectors also reviewed the
    licensees issue report database to determine if any problems had been identified with
    the PI data collected or transmitted for this indicator and none were identified.
    Documents reviewed are listed in the Attachment to this report.
    This inspection constituted two MSPI cooling water system samples as defined in
    IP 71151-05.
  b. Findings
    No findings of significance were identified.
.6  Reactor Coolant System Specific Activity
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Reactor Coolant System (RCS)
    Specific Activity PI for the period from July 2009 through September 2010. The
    inspectors used PI definitions and guidance contained in the NEI 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 6, dated October 2009, to
    determine the accuracy of the PI data reported during those periods. The inspectors
    reviewed the licensees RCS chemistry samples, TS requirements, issue reports, event
    reports, and NRC Integrated IRs for the period of July 2009 through September 2010 to
    determine if indicator results were accurately reported. Documents reviewed are listed
    in the Attachment to this report
    This inspection constituted two reactor coolant systems specific activity sample as
    defined in IP 71151-05.
                                            24                                Enclosure


The BFP FH-71 contained guidance of when to initiate temperature monitoring of the annulus region; however the procedure failed to contain guidance of when
  b. Findings
    No findings of significance were identified.
.7  Occupational Exposure Control Effectiveness
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Occupational Radiological
    Occurrences PI for the period of July 2009 through September 2010. The inspectors
    used PI definitions and guidance contained in the NEI 99-02, Regulatory Assessment
    Performance Indicator Guideline, Revision 6, dated October 2009, to determine the
    accuracy of the PI data reported during those periods. The inspectors reviewed
    electronic dosimetry dose rate and accumulated dose alarm and dose reports and the
    dose assignments for any intakes that occurred for selected dates between July 2009
    and September 2010 to determine if indicator results were accurately reported. The
    inspectors also conducted walk downs of numerous locked high and very high radiation
    area entrances to determine the adequacy of the controls in place for these areas.
    Documents reviewed are listed in the Attachment to this report.
    This inspection constituted one occupational radiological occurrences sample as defined
    in IP 71151-05.
  b. Findings
    No findings of significance were identified.
.8  Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
    Radiological Effluent Occurrences
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Radiological Effluent Technical
    Specification (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent
    Occurrences performance indicator for the period of July 2009 through September 2010.
    The inspectors used PI definitions and guidance contained in the NEI 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 6, dated October 2009, to
    determine the accuracy of the PI data reported during those periods. The inspectors
    reviewed the licensees issue report database and selected individual reports generated
    since this indicator was last reviewed to identify any potential occurrences such as
    unmonitored, uncontrolled, or improperly calculated effluent releases that may have
    impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the
    results of associated offsite dose calculations for selected dates from July 2009 through
    September 2010 to determine if indicator results were accurately reported. The
    inspectors also reviewed the licensees methods for quantifying gaseous and liquid
    effluents and determining effluent dose. Documents reviewed are listed in the
    Attachment to this report.
    This inspection constituted one RETS/ODCM radiological effluent occurrences sample
    as defined in IP 71151-05.
                                            25                                Enclosure


temperature monitoring was to be terminated. On October 17, 2010, during MPC
  b. Findings
processing operations, the licensee completed vacuum drying operations and  
      No findings of significance were identified.
subsequently terminated, without procedural guidance, monitoring of annulus temperature. At the time monitoring was terminated, the canister was still under vacuum and annulus temperature requirements were still required by the licensee's
4OA2 Identification and Resolution of Problems (71152)
design basis. The inspectors brought this discrepancy to the attention of the field
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
supervisor and the licensee reinitiated temperature monitoring until the MPC was
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
filled with helium. The licensee entered this issue into in its CAP (IR 1131564) and
      Physical Protection
completed procedural revisions.  
.1  Routine Review of Items Entered into the Corrective Action Program
3. The BFP FH-71, "MPC Processing," Revision 8, provides guidance for the licensee to complete MPC processing operations.   
  a. Inspection Scope
On October 15, 2010, an unanalyzed condition was identified regarding spent fuel peak cladding temperatures while a MPC was filled with nitrogen. The Holtec FSAR Revision 5 has a thermal analysis for water, helium, and vacuum to exist in the MPC,
      As part of the various baseline inspection procedures discussed in previous sections of
however nitrogen, which is used to force water out of the MPC and provide a
      this report, the inspectors routinely reviewed issues during baseline inspection activities
temporary inert atmosphere prior to vacuum drying, is unanalyzed. The procedures
      and plant status reviews to verify that they were being entered into the licensees CAP at
section of the Holtec FSAR stated that helium or nitrogen can be used as a gas for
      an appropriate threshold, that adequate attention was being given to timely corrective
      actions, and that adverse trends were identified and addressed. Attributes reviewed
      included: the complete and accurate identification of the problem; that timeliness was
      commensurate with the safety significance; that evaluation and disposition of
      performance issues, generic implications, common causes, contributing factors, root
      causes, extent-of-condition reviews, and previous occurrences reviews were proper and
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
      Minor issues entered into the licensees CAP as a result of the inspectors observations
      are included in the attached List of Documents Reviewed.
      These routine reviews for the identification and resolution of problems did not constitute
      any additional inspection samples. Instead, by procedure they were considered an
      integral part of the inspections performed during the quarter and documented in
      Section 1 of this report.
  b. Findings
      No findings of significance were identified.
  .2   Daily Corrective Action Program Reviews
  a. Inspection Scope
      In order to assist with the identification of repetitive equipment failures and specific
      human performance issues for follow-up, the inspectors performed a daily screening of
      items entered into the licensees CAP. This review was accomplished through
      inspection of the stations daily condition report packages.
      These daily reviews were performed by procedure as part of the inspectors daily plant
      status monitoring activities and, as such, did not constitute any separate inspection
      samples.
                                              26                                  Enclosure


water blowdown operations; however the FSAR did not provide a thermal analysis for nitrogen. The licensee failed to have an independent thermal analysis for this condition. The licensee determined that the vacuum thermal analysis bounded the  
b. Findings
condition; however this analysis required annulus cooling and imposed MPC shell  
    No findings of significance were identified.
33 Enclosure
.3  Semi Annual Trend Review
  temperature limits. The licensee initiated annulus cooling, however when the system actuated, the MPC shell temperature design limit of 125°F was exceeded by several
a. Inspection Scope
degrees.  Several hours later, the licensee lost function of a chiller in support of annulus cooling which caused the FSAR temperature limit of 125°F to again be exceeded for a short period of time. The licensee implemented contingency actions  
    The inspectors performed a review of the licensees CAP and associated documents to
    identify trends that could indicate the existence of a more significant safety issue. The
    inspectors review was focused on repetitive equipment issues, but also considered the
    results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
    licensee trending efforts, and licensee human performance results. The inspectors
    review nominally considered the 6 month period of June 1, 2010, through
    November 30, 2010, although some examples expanded beyond those dates where the
    scope of the trend warranted.
    The review also included issues documented outside the normal CAP; including major
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
    problem/challenges lists, system health reports, quality assurance audit/surveillance
    reports, self assessment reports, and Maintenance Rule assessments. The inspectors
    compared and contrasted their results with the results contained in the licensees
    CAP trending reports. Corrective actions associated with a sample of the issues
    identified in the licensees trending reports were reviewed for adequacy.
    This review constituted a single semi-annual trend inspection sample as defined in
    IP 71152-05.
  b. Findings
    No findings of significance were identified.
.4  Annual Sample: Review of Operator Workarounds
  a. Inspection Scope
    The inspectors evaluated the licensees implementation of their process used to identify,
    document, track, and resolve operational challenges. Inspection activities included, but
    were not limited to, a review of the cumulative effects of the Operator Workarounds
    (OWAs) on system availability and the potential for improper operation of the system, for
    potential impacts on multiple systems, and on the ability of operators to respond to plant
    transients or accidents.
    The inspectors performed a review of the cumulative effects of OWAs. The documents
    listed in the Attachment were reviewed to accomplish the objectives of the inspection
    procedure. The inspectors reviewed both current and historical operational challenge
    records to determine whether the licensee was identifying operator challenges at an
    appropriate threshold, had entered them into their CAP, and proposed or implemented
    appropriate and timely corrective actions which addressed each issue. Reviews were
    conducted to determine if any operator challenge could increase the possibility of an
    initiating event, if the challenge was contrary to training, required a change from
    long-standing operational practices, or created the potential for inappropriate
                                            27                                  Enclosure


for the annulus chiller failure, which consisted of a feed of plant demineralized water into the annulus region and out to plant water treatment to reduce the temperature.  
      compensatory actions. Additionally, all temporary modifications were reviewed to
      identify any potential effect on the functionality of Mitigating Systems, impaired access to
The licensee failed to maintain MPC shell temperatures in accordance with an associated bounding design basis. The licensee entered this issue into its corrective action program (IR 1127060).  Following the event, the licensee contacted
      equipment, or required equipment uses for which the equipment was not designed.
the cask vendor, Holtec, and completed an analysis to show that peak fuel cladding
      Daily plant and equipment status logs, degraded instrument logs, and operator aids or
temperature limits were not exceeded and initiated procedural changes.
      tools being used to compensate for material deficiencies were also assessed to identify
Analysis:  The inspectors determined that the licensee's failure to have adequate procedures was a violation that warranted a significance evaluation. Consistent with the  
      any potential sources of unidentified operator workarounds.
guidance in Section 2.2 of the NRC Enforcement Policy, ISFSIs are not subject to the SDP and, thus, traditional enforcement will be used for these facilities. The violation was dispositioned using the traditional enforcement process using Section 2.3 of the  
      This review constituted one operator workaround annual inspection sample as defined in
      IP 71152-05.
  b. Findings
      No findings of significance were identified.
4OA3 Followup of Events and Notices of Enforcement Discretion (71153)
.1  (Closed) Licensee Event Report 05000455/2010-001-00: Reactor Protection and
      Auxiliary Feedwater Actuation Signals from Low Steam Generator (S/G) Level Due to
      Inadequate Surveillance Testing
      On April 19, 2010, Unit 2 was in the process of shutting down and cooling down in order
      to enter a planned refuelling outage. At 5:03 am with the unit in Mode 4, Hot Shutdown,
      a feedwater isolation valve (FWIV) surveillance was in progress and the 2D S/G
      secondary side water level lowered to the low S/G water level setpoint, which resulted in
      a valid FWIV actuation. All equipment actuated properly and due to the plant condition,
      the control rods were already fully inserted with the reactor trip breakers open.
      The licensees apparent cause evaluation determined that the operators had received
      Just-In-Time training immediately prior to the refuelling outage. However, inadequate
      oversight combined with an inadequate procedure had resulted in inadequate control of
      the surveillance test activity. The licensee determined that the surveillance procedure
      did not allow for S/G levels to be recovered between the testing of the two trains,
      performance of the test during the outage was not performed at the optimum time based
      on plant parameters, and no pre-job briefing was performed the night of the test. The
      licensee had determined that while the test was performed during a time in the outage
      that it was usually performed that it had been performed when the RCS was hotter than
      it had been before, which resulted in the S/G water level steaming off at a faster rate
      than previously experienced.
      The inspectors reviewed the Licensee Event Report (LER), licensee procedures, and
      performed interviews of selected licensee personnel. The inspectors agreed with the
      licensees apparent cause evaluation conclusion regarding the three causes of the FWIV
      actuation. The inspectors reviewed the licensees corrective actions and verified that the
      corrective actions addressed the causes and were implemented. Corrective actions
      included revising the FWIV surveillance procedure, strengthening pre-job briefs, and
      reinforcing the roles and responsibilities of key outage operations positions.
      Although this issue was corrected, it constituted a performance deficiency and a minor
      violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and
      Drawings. However, it is not subject to enforcement action in accordance with
      Section 2.3.1 of the Enforcement Policy. Because the performance deficiency was not
                                              28                                  Enclosure


Enforcement Policy.   
      more than minor and not a finding per IMC 0612, Appendix B, Issue Screening, a
      cross-cutting aspect was not assigned to this violation.
      This event follow-up review constituted one sample as defined in IP 71153-05.
4OA5 Other Activities
.1  Review of Institute of Nuclear Power Operations Report
      The inspectors reviewed the Institute of Nuclear Power Operations July 2010 Evaluation
      Report, Byron Station, dated December 10, 2010.
   .2  Operation of an Independent Spent Fuel Storage Installation at Operating Plants
      (60855.1)
  a. Inspection Scope
      The inspectors observed and evaluated the licensees loading operations of the first and
      second multi-purpose canisters (MPC) during the licensees initial spent fuel loading
      campaign to verify compliance with the Certificate of Compliance, TS, NRC Regulations,
      and associated procedures. The inspectors observed heavy loads movements inside
      the Fuel Handling Building (FHB) including: lifting of the transfer cask (HI-TRAC) into the
      spent fuel pool, lifting of the HI-TRAC from the spent fuel pool to the decontamination
      stand, and transfer of the MPC from the HI-TRAC to the storage cask (HI-STORM) while
      the casks are stacked on one another in a laterally restrained configuration. The
      inspectors observed loading of spent fuel assemblies from the spent fuel pool into the
      MPC. The inspectors observed MPC processing operations including: decontamination
      and surveying, canister welding, non-destructive weld examinations, hydrostatic testing,
      canister draining, vacuum drying, and helium backfilling. The inspectors observed heavy
      loads operations outside of the FHB including: transfer of the HI-STORM from inside of
      the FHB to outside of the FHB on a low profile transporter, and transfer of the
      HI-STORM to the Independent Spent Fuel Storage Installation (ISFSI) pad using a
      vertical cask transporter.
      During performance of the activities, the inspectors evaluated the licensee staffs
      familiarity with procedures, supervisory oversight, and communication and coordination
      between the different groups involved. The inspectors reviewed loading procedures and
      evaluated the licensees adherence to these procedures. The inspectors also observed
      the licensees process to verify that the contamination and radiation levels from the
      transfer cask and storage cask were below the regulatory and TS limits. The inspectors
      attended various pre-job briefs to assess the licensees ability to identify critical steps of
      the evolution, potential failure scenarios, and tools to prevent errors.
      The inspectors reviewed issue reports and the associated follow-up actions that were
      generated during the loading campaign as well as 10 CFR 72.48 screenings.
      On Saturday, August 28, 2010, the licensees first MPC containing spent nuclear fuel
      was left unmonitored during processing operations at the end-of-shift operations. The
      MPC had been undergoing vacuum drying throughout the day and at the end of shift
      was left under vacuum. While the canister was under vacuum, cooling of the fuel was
      significantly reduced, and subsequently fuel temperatures were elevated. The licensees
                                            29                                  Enclosure


    safety analysis for the spent fuel cask system required that the MPC shell temperature
Example 1 was determined to be of more than minor significance using IMC 0612,  
    be maintained below 125 degrees Fahrenheit (°F) while the MPC is under vacuum. A
"Power Reactor Inspection Reports," Appendix E, "Examples of Minor Issues," Example 3i, in that the licensee's lack of evaluation did not assure spent fuel cladding temperatures during vacuum drying would remain less than SFST ISG-11 safety limits and an additional calculation was required to evaluate the condition. Examples 2 and 3
    MPC shell temperature of 125°F corresponds to a design basis limit of 1040°F for fuel
were determined to be of more than minor significance using IMC 0612, "Power Reactor
    cladding temperature as discussed in the Holtec HI-STORM 100 FSAR, Revision 5.
Inspection Reports," Appendix E, "Examples of Minor Issues," Example 2c, in that the procedures failed to incorporate thermal acceptance criteria established by the FSAR and that the failure to incorporate thermal acceptance criteria was repetitive.  
    Cooling of the water contained within the HI-TRAC annulus, the area between the MPC
    and the HI-TRAC, is provided by a chiller unit when required. For the fuel selected,
    annulus cooling would be required to maintain the MPC shell temperature below 125oF.
    Prior to the end of shift on August 28, 2010, the inspectors asked the licensee what
    plans were in place for monitoring the MPC overnight. The inspectors were informed
    that various options were being considered for monitoring the MPC overnight and that a
    final decision on the exact method of monitoring and specific staffing had not been
    determined. Later that evening, the licensee discussed the importance of the chiller with
    technical experts and determined that, due to the heat loads selected for this canister,
    heat rates were not high enough to exceed fuel temperature limits even in the event of a
    chiller shut off. Therefore, the licensee concluded that no monitoring was necessary
    overnight. No specific analysis was performed to support this determination.
    On the morning of August 29, 2010, the licensee identified that the chiller had
    unexpectedly shut off overnight; however, the licensee failed to recognize that the
    annulus water temperature corresponded to a safety limit for fuel cladding temperature
    as discussed in the FSAR. A back-up chiller was placed in service promptly; however,
    the licensee did not recognize the importance of determining the current water
    temperature to ensure that no safety limits were exceeded. The inspectors notified the
    licensee of the design basis annulus water temperature limit of 125oF, which was
    specified in the FSAR. The inspectors estimated that the 125oF limit was likely
    exceeded by several degrees.
    The licensee began a prompt evaluation to determine if any fuel cladding safety limits
    were exceeded. Working with the licensees vendor, Holtec, the prompt evaluation
    concluded that no fuel cladding safety limits were exceeded.
    In response to the circumstances of August 28 and 29, 2010, the NRC increased the
    oversight of the ISFSI project at the Byron Station and began a reactive inspection on
    September 1, 2010. The results of this reactive inspection are documented in NRC
    IR Nos. 05000454/2010007; 05000455/2010007; and 07200068/2010002.
    Following completion of the reactive inspection the inspectors reviewed the licensees
    corrective actions that had been completed and subsequent procedure changes. The
    ISFSI inspectors remained onsite for the licensees second MPC loading operations.
    Following the second MPC loading, ISFSI inspectors monitored loading operations from
    the regional office.
b.  Findings
(1) Inadequate Procedures for Implementing Final Safety Analysis Report Required Annulus
    Cooling
    Introduction: The inspectors identified a Severity Level IV NCV of very low safety
    significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings." Specifically,
                                          30                                Enclosure


the licensee failed to have procedures in place to ensure that the design basis peak fuel
Consistent with the guidance in Section 2.6.D of the NRC Enforcement Manual, if a  
cladding temperature limit would not be exceeded during canister loading operations.
violation does not fit an example in the Enfo
Description: The licensee revised their ISFSI loading procedures following the
rcement Policy Violation Examples, it should be assigned a severity level:  (1) commensurate with its safety significance; and  (2) informed by similar violations addressed in the Violation Examples. The inspectors found no similar violations in the Violation Examples.  Subsequent analysis by the  
circumstances of August 28 and 29. During review of the revised procedures, the
licensee indicated that fuel cladding temperature safety limits were not exceeded;  
inspectors identified three examples where the licensee failed to meet the requirements
therefore, the violation was determined to be of very low safety significance (Severity
in 10 CFR 72.150, Instructions, Procedures, and Drawings.
1. Byron Fuel Handling Procedure BFP FH-71, MPC Processing, Revision 8, provides
    guidance for the licensee to complete MPC processing operations.
    The Holtec FSAR, Revision 5, Chapter 4, discussed how the fuel cladding
    temperature limits and associated hoop stress calculation requirements were
    consistent with the guidance in Spent Fuel Storage and Transportation (SFST)
    Interim Staff Guidance (ISG) - 11 during vacuum drying operations. Specifically, the
    Holtec FSAR, Revision 5, Section 4.5.1.1.4.1, Vacuum Drying states, in part:
        The initial loading of Spent Nuclear Fuel in the MPC requires that the water
        within the MPC be drained and replaced with helium. For MPCs containing
        moderate burn-up fuel assemblies only, this operation may be carried out using
        the conventional vacuum drying approach. In this method, removal of the last
        traces of residual moisture from the MPC cavity is accomplished by evacuating
        the MPC for a short time after draining the MPC.
        For any decay heat load in an MPC-32, vacuum drying of the MPC is performed
        with the annular gap between the MPC and the HI-TRAC continuously flushed
        with water. The water movement in this annular gap will maintain the MPC shell
        temperature at about the temperature of flowing water. Thus, the thermal
        analysis of the MPC during vacuum drying for these conditions is performed with
        cooling of the MPC shell with water at a bounding maximum temperature of
        125oF.
        To avoid excessive conservatism in the computed FLUENT solution, partial
        recognition for higher axial heat dissipation is adopted in the peak cladding
        calculations. The boundary conditions applied to this evaluation are: ii. The
        entire outer surface of the MPC shell is postulated to be at a bounding maximum
        temperature of 125°F.
    As described in the Holtec FSAR, the intent of flushing water through the annulus
    region between the HI-TRAC and the MPC is to maintain the surface of the MPC
    shell below 125 °F. The Holtec FSAR states that if MPC shell temperature remains
    below 125 °F, the peak fuel cladding temperatures, for moderate burn-up fuel, during
    short-term vacuum drying operations, in an MPC with design basis maximum heat
    loads, are calculated to be less than the SFST ISG-11 safety limit of 1058ºF.
    During vacuum drying operations at the Byron Station, the seal that maintains water
    inside the annulus region is removed and allowed to flood several inches over the
    top of the MPC. The licensees procedures required the annulus water to be cooled
    with a submersible pump, heat exchanger, and chiller. The submersible pump took a
    suction of water above the MPC lid and discharged water on the other side of the
                                      31                                  Enclosure


Level IV).  
  MPC lid. Temperature measurements were recorded near the suction and discharge
Enforcement:  10 CFR 72.150, "Instructions, Procedures, and Drawings," states, in part, that the licensee shall prescribe activities affecting quality by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall require that these instructions, procedures, and drawings be followed. The instructions, procedures,  
  locations. The licensee failed to have an analysis demonstrating that temperatures
and drawings must include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished.
  measured at the top of the MPC where water was being continuously flushed by a
  submersible pump was indicative of canister shell temperatures on the side of the
 
  MPC where water was not being continuously flushed. The licensee failed to
34 Enclosure
  configure the intake and discharge of the submersible pump to ensure that all
Contrary to the above,  1. On October 15, 2010, Procedure BFP FH-71, "MPC Processing," Revision 8, was identified to not contain adequate instructions, since the procedure failed to configure
  regions of the MPC were continuously flushed with water and subsequently failed to
the intake and discharge of the submersible pump to ensure that all regions of the MPC were continuously being flushed with water and subsequently failed to ensure
  ensure that temperature measurements taken were indicative of the highest shell
that temperature measurements taken were indicative of the highest MPC shell  
  temperatures present. The licensee entered these issues into its CAP (IR 1131564)
  and initiated actions to evaluate the condition. Following the event, the licensee
  contacted the cask vendor, Holtec, and completed an analysis to show that peak fuel
  cladding temperature limits were not exceeded. The licensee revised the
  configuration of the pump such that the pump intake was at the top of the annulus
  and the pump discharge was through the annulus drain line near the bottom of the
  annulus.
2. The BFP FH-71, MPC Processing, Revision 8, provides guidance for the licensee
  to complete MPC processing operations.
  As previously discussed in 4OA5.2.b.1.1, the annulus between the MPC and the
  HI-TRAC is required to be continuously flushed with water to ensure that the MPC
  shell temperature is maintained below the design basis limit of 125 oF in order to
  maintain fuel cladding peak temperatures under design limits as described in the
  Holtec FSAR, Revision 5.
  The BFP FH-71 contained guidance of when to initiate temperature monitoring of the
  annulus region; however the procedure failed to contain guidance of when
  temperature monitoring was to be terminated. On October 17, 2010, during MPC
  processing operations, the licensee completed vacuum drying operations and
  subsequently terminated, without procedural guidance, monitoring of annulus
  temperature. At the time monitoring was terminated, the canister was still under
  vacuum and annulus temperature requirements were still required by the licensees
  design basis. The inspectors brought this discrepancy to the attention of the field
  supervisor and the licensee reinitiated temperature monitoring until the MPC was
  filled with helium. The licensee entered this issue into in its CAP (IR 1131564) and
  completed procedural revisions.
3. The BFP FH-71, MPC Processing, Revision 8, provides guidance for the licensee
  to complete MPC processing operations.
  On October 15, 2010, an unanalyzed condition was identified regarding spent fuel
  peak cladding temperatures while a MPC was filled with nitrogen. The Holtec FSAR
  Revision 5 has a thermal analysis for water, helium, and vacuum to exist in the MPC,
  however nitrogen, which is used to force water out of the MPC and provide a
  temporary inert atmosphere prior to vacuum drying, is unanalyzed. The procedures
  section of the Holtec FSAR stated that helium or nitrogen can be used as a gas for
  water blowdown operations; however the FSAR did not provide a thermal analysis
  for nitrogen. The licensee failed to have an independent thermal analysis for this
  condition. The licensee determined that the vacuum thermal analysis bounded the
  condition; however this analysis required annulus cooling and imposed MPC shell
                                      32                                  Enclosure


temperatures present.
    temperature limits. The licensee initiated annulus cooling, however when the system
  2. On October 15, 2010, Procedure BFP FH-71, "MPC Processing," Revision 8, was identified to not contain adequate instructions, since the procedure failed to contain guidance of when temperature monitoring was to be terminated. During MPC
    actuated, the MPC shell temperature design limit of 125°F was exceeded by several
processing operations, the licensee completed vacuum drying operations and  
    degrees. Several hours later, the licensee lost function of a chiller in support of
subsequently terminated, without procedural guidance, monitoring of annulus
    annulus cooling which caused the FSAR temperature limit of 125°F to again be
    exceeded for a short period of time. The licensee implemented contingency actions
    for the annulus chiller failure, which consisted of a feed of plant demineralized water
    into the annulus region and out to plant water treatment to reduce the temperature.
      The licensee failed to maintain MPC shell temperatures in accordance with an
      associated bounding design basis. The licensee entered this issue into its
      corrective action program (IR 1127060). Following the event, the licensee contacted
      the cask vendor, Holtec, and completed an analysis to show that peak fuel cladding
      temperature limits were not exceeded and initiated procedural changes.
Analysis: The inspectors determined that the licensees failure to have adequate
procedures was a violation that warranted a significance evaluation. Consistent with the
guidance in Section 2.2 of the NRC Enforcement Policy, ISFSIs are not subject to the
SDP and, thus, traditional enforcement will be used for these facilities. The violation was
dispositioned using the traditional enforcement process using Section 2.3 of the
Enforcement Policy.
Example 1 was determined to be of more than minor significance using IMC 0612,
Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues,
Example 3i, in that the licensees lack of evaluation did not assure spent fuel cladding
temperatures during vacuum drying would remain less than SFST ISG-11 safety limits
and an additional calculation was required to evaluate the condition. Examples 2 and 3
were determined to be of more than minor significance using IMC 0612, Power Reactor
Inspection Reports, Appendix E, Examples of Minor Issues, Example 2c, in that the
procedures failed to incorporate thermal acceptance criteria established by the FSAR
and that the failure to incorporate thermal acceptance criteria was repetitive.
Consistent with the guidance in Section 2.6.D of the NRC Enforcement Manual, if a
violation does not fit an example in the Enforcement Policy Violation Examples, it should
be assigned a severity level: (1) commensurate with its safety significance; and
(2) informed by similar violations addressed in the Violation Examples. The inspectors
found no similar violations in the Violation Examples. Subsequent analysis by the
licensee indicated that fuel cladding temperature safety limits were not exceeded;
therefore, the violation was determined to be of very low safety significance (Severity
Level IV).
Enforcement: 10 CFR 72.150, Instructions, Procedures, and Drawings, states, in part,
that the licensee shall prescribe activities affecting quality by documented instructions,
procedures, or drawings of a type appropriate to the circumstances and shall require that
these instructions, procedures, and drawings be followed. The instructions, procedures,
and drawings must include appropriate quantitative or qualitative acceptance criteria for
determining that important activities have been satisfactorily accomplished.
                                        33                                Enclosure


temperatures when annulus temperature requirements were still required by the licensee's design basis.  
    Contrary to the above,
3. On October 15, 2010, Procedure BFP FH-71, "MPC Processing," Revision 8, was identified to not contain adequate instructions, since the procedure failed to maintain MPC shell temperatures in accordance with an associated bounding design basis analysis while the MPC was filled with nitrogen.  
    1. On October 15, 2010, Procedure BFP FH-71, MPC Processing, Revision 8, was
        identified to not contain adequate instructions, since the procedure failed to configure
        the intake and discharge of the submersible pump to ensure that all regions of the
        MPC were continuously being flushed with water and subsequently failed to ensure
        that temperature measurements taken were indicative of the highest MPC shell
        temperatures present.
    2. On October 15, 2010, Procedure BFP FH-71, MPC Processing, Revision 8, was
        identified to not contain adequate instructions, since the procedure failed to contain
        guidance of when temperature monitoring was to be terminated. During MPC
        processing operations, the licensee completed vacuum drying operations and
        subsequently terminated, without procedural guidance, monitoring of annulus
        temperatures when annulus temperature requirements were still required by the
        licensees design basis.
    3. On October 15, 2010, Procedure BFP FH-71, MPC Processing, Revision 8, was
        identified to not contain adequate instructions, since the procedure failed to maintain
        MPC shell temperatures in accordance with an associated bounding design basis
        analysis while the MPC was filled with nitrogen.
    This is a violation of 10 CFR 72.150, Instructions, Procedures, and Drawings. This
    Severity Level IV Violation is being treated as a NCV consistent with Section 3.1.1 of the
    NRC Enforcement Manual. The licensee documented these issues in its corrective
    action program as IR 1131564 and IR 1127060. (NCV 05000454/2010005-02;
    05000455/2010005-02; 07200068/2010003-1, Inadequate Procedures for
    Implementing FSAR Required Annulus Cooling)
(2) Inadequate Procedural Guidance for Heavy Loads Operations
    Introduction: The inspectors identified a Severity Level IV NCV of very low safety
    significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings." Specifically,
    the licensee failed to have procedures in place to ensure that heavy loads were operated
    safely in the Fuel Handling Building.
    Description: The inspectors identified two examples where the licensee failed to meet
    the requirements of 10 CFR 72.150, Instructions, Procedures, and Drawings.
    1. On August 24, 2010, the inspectors observed that the crane operator did not check
        the hoist brakes on the Fuel Handling Building crane while lifting a HI-TRAC and an
        empty MPC from the decontamination stand to the cask wet pit in the spent fuel pool.
        The lifted load at the time was approximately 90 tons. The next load to be lifted, a
        HI-TRAC with a fully loaded MPC, would be just under the maximum critical load of
        the crane, 125 tons.
        The Byron Station is committed to following the requirements of ASME B30.2.0-
        1976, Overhead and Gantry Cranes (Top Running Bridge, Multiple Girder). In
        ASME B30.2.0-1976, Section 2-3.2.3.g, it states The operator shall check the hoist
                                          34                                Enclosure


This is a violation of 10 CFR 72.150, "Instructions, Procedures, and Drawings."  This
    brakes at least once each shift if a load approaching the rated load is to be handled.
Severity Level IV Violation is being treated as a NCV consistent with Section 3.1.1 of the NRC Enforcement Manual. The licensee documented these issues in its corrective action program as IR 1131564 and IR 1127060. (NCV 05000454/2010005-02; 05000455/2010005-02; 07200068/2010003-1, Inadequate Procedures for
    This shall be done by raising the load a short distance and applying the brakes.
Implementing FSAR Required Annulus Cooling)
    The inspectors brought the requirements of ASME B30.2.0-1976 to the attention of
(2) Inadequate Procedural Guidance for Heavy Loads Operations
    the field supervisor and the crane operator checked the crane brakes. The
  Introduction:  The inspectors identified a Severity Level IV NCV of very low safety significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings."  Specifically, the licensee failed to have procedures in place to ensure that heavy loads were operated safely in the Fuel Handling Building.
    inspectors reviewed licensee procedures related to heavy loads operations and
    determined that no procedural guidance existed to instruct crane operators to check
    holding brakes or defined a specific weight as approaching the rated load. The
    licensee documented the issue in its corrective action program (IR 1106006), and
    added procedural guidance.
2. On September 4, 2010, the licensee was performing MPC transfer operations from
    the HI-TRAC to the HI-STORM in a restrained stack configuration using BFP FH-69,
    HI-TRAC Movement within the Fuel Building, Revision 5. During withdrawal of the
    mating device tongue, the bottom HI-TRAC pool lid became mispositioned in the
    mating device when one of the air bags did not fully deflate. The licensee was
    unaware this mispositioning placed the edge of the HI-TRAC pool lid in the travel
    path of the MPC when it was to be downloaded. The licensee continued and began
    to lower the MPC from the HI-TRAC into the HI-STORM. The inspectors observed
    that a momentary unexpected load decrease was registered on the Fuel Handling
    Building crane load cell from approximately 38 tons to approximately 19 tons. As the
    signalman instructed the crane operator to cease lowering, a loud noise was heard,
    and the load cell indicated a rapid rise in load back up to approximately 38 tons.
    Heavy loads operations were immediately stopped, and plant notifications were
    made. The licensee determined that the safest configuration for the MPC would be
    inside the HI-STORM and subsequently continued the transfer operation. The
    HI-TRAC pool lid had damage to its protective coating. The licensee performed a
    walkdown of the crane, inspected the slings for damage, and performed a structural
    analysis to show that the MPC could still perform its design function. The licensee
    failed to have procedures in place to ensure the mating device air bags properly
    deflated and that the HI-TRAC pool lid was correctly positioned on the mating device.
    The licensee failed to have procedures that would ensure that interference points
    such as the HI-TRAC bottom pool lid did not exist during MPC transfer operations.
    The licensee documented the issue in its corrective action program (IR 1109925),
    and added procedural guidance.
Analysis: The inspectors determined that the licensees failure to have adequate
procedures was a violation that warranted a significance evaluation. Consistent with the
guidance in Section 2.2 of the NRC Enforcement Policy, ISFSIs are not subject to the
SDP and, thus, traditional enforcement will be used for these facilities. The violation was
dispositioned using the traditional enforcement process using Section 2.3 of the
Enforcement Policy.
The examples were determined to be of more than minor significance because if left
uncorrected, these could lead to a more significant safety concern. Consistent with the
guidance in Section 2.6.D of the NRC Enforcement Manual, if a violation does not fit an
example in the Enforcement Policy Violation Examples, it should be assigned a severity
level: (1) Commensurate with its safety significance; and (2) informed by similar
violations addressed in the Violation Examples. The violation screened as having very
low safety significance (Severity Level IV).
                                      35                                Enclosure


Description: The inspectors identified two examples where the licensee failed to meet the requirements of 10 CFR 72.150, "Instructions, Procedures, and Drawings." 1. On August 24, 2010, the inspectors observed that the crane operator did not check the hoist brakes on the Fuel Handling Building crane while lifting a HI-TRAC and an
    Enforcement: 10 CFR 72.150, Instructions, Procedures, and Drawings, states, in part,
empty MPC from the decontamination stand to the cask wet pit in the spent fuel pool. 
    that the licensee shall prescribe activities affecting quality by documented instructions,
The lifted load at the time was approximately 90 tons. The next load to be lifted, a
    procedures, or drawings of a type appropriate to the circumstances and shall require that
HI-TRAC with a fully loaded MPC, would be just under the maximum critical load of
    these instructions, procedures, and drawings be followed. The instructions, procedures,
the crane, 125 tons.
    and drawings must include appropriate quantitative or qualitative acceptance criteria for
The Byron Station is committed to following the requirements of ASME B30.2.0-
    determining that important activities have been satisfactorily accomplished.
1976, "Overhead and Gantry Cranes (Top Running Bridge, Multiple Girder)." In
    Contrary to the above,
ASME B30.2.0-1976, Section 2-3.2.3.g, it states "The operator shall check the hoist 
    1. On August 24, 2010, Procedure FH-20; Operation of Fuel Handling Building Crane;
35 Enclosure
        Revision 24, was identified to not contain adequate instructions, since the procedure
brakes at least once each shift if a load approaching the rated load is to be handled. This shall be done by raising the load a short distance and applying the brakes.
        failed to establish procedural guidance to instruct crane operators to check holding
        brakes or define a specific weight as approaching a rated load. The licensee
        documented the issue in its corrective action program.
    2. On September 4, 2010, Procedure BFP FH-69, HI-TRAC Movement within the Fuel
        Building, Revision 5, was identified to not contain adequate instruction, since the
        procedure failed to have steps in place to ensure the mating device air bags properly
        deflated and that the HI-TRAC pool lid was correctly positioned on the mating device.
        The licensee failed to have procedures that would ensure that interference points
        such as the HI-TRAC bottom pool lid did not exist during MPC transfer operations.
    This is a violation of 10 CFR 72.150, Instructions, Procedures, and Drawings. This
    Severity Level IV Violation is being treated as a NCV consistent with Section 3.1.1 of the
    NRC Enforcement Manual. The licensee documented these issues in its corrective
    action program as IR1106006 and IR1109925. (NCV 05000454/2010005-03;
    05000455/2010005-03; 07200068/2010003-2, Inadequate Procedural Guidance for
    Heavy Loads Operations.)
4OA6 Meetings
.1 Exit Meeting Summary
    On January 13, 2011, the inspectors presented the inspection results to Mr. B. Adams,
    and other members of the licensee staff. The licensee personnel acknowledged the
    inspection results presented. The inspectors confirmed that all proprietary material
    reviewed during the inspection was returned to the licensee staff.
.2 Interim Exit Meetings
    Interim exits were conducted for:
    *        The results of the LORT Program inspection with Ms. L. Bogue on October 29,
              2010.
    *        The results of the Heat Sink inspection to Mr. B. Adams on December 3, 2010.
    *        The results of the Radioactive Gaseous and Liquid Effluent Treatment and
              Performance Indicator Verification inspection with Mr. D. Enright on
              December 14, 2010.
                                            36                                Enclosure


The inspectors brought the requirements of ASME B30.2.0-1976 to the attention of the field supervisor and the crane operator checked the crane brakes.  The
    *      The results of the ISFSI Initial Cask Loading Campaign inspection with
inspectors reviewed licensee procedures related to heavy loads operations and
            Mr. D. Enright on December 20, 2010.
determined that no procedural guidance existed to instruct crane operators to check
    The licensee acknowledged the issues presented. The inspectors confirmed that none
holding brakes or defined a specific weight as "approaching the rated load."  The
    of the potential report input discussed was considered proprietary.
licensee documented the issue in its corrective action program (IR 1106006), and added procedural guidance.  
ATTACHMENT: SUPPLEMENTAL INFORMATION
2. On September 4, 2010, the licensee was performing MPC transfer operations from the HI-TRAC to the HI-STORM in a restrained stack configuration using BFP FH-69,
                                            37                            Enclosure
"HI-TRAC Movement within the Fuel Building," Revision 5.  During withdrawal of the mating device tongue, the bottom HI-TRAC pool lid became mispositioned in the mating device when one of the air bags did not fully deflate. The licensee was
unaware this mispositioning placed the edge of the HI-TRAC pool lid in the travel
path of the MPC when it was to be downloaded.  The licensee continued and began
to lower the MPC from the HI-TRAC into the HI-STORM. The inspectors observed that a momentary unexpected load decrease was registered on the Fuel Handling Building crane load cell from approximately 38 tons to approximately 19 tons.  As the
signalman instructed the crane operator to cease lowering, a loud noise was heard,
and the load cell indicated a rapid rise in load back up to approximately 38 tons. 
Heavy loads operations were immediately stopped, and plant notifications were
made.  The licensee determined that the safest configuration for the MPC would be inside the HI-STORM and subsequently continued the transfer operation.  The HI-TRAC pool lid had damage to its protective coating.  The licensee performed a
walkdown of the crane, inspected the slings for damage, and performed a structural
analysis to show that the MPC could still perform its design function.  The licensee
failed to have procedures in place to ensure the mating device air bags properly deflated and that the HI-TRAC pool lid was correctly positioned on the mating device.  The licensee failed to have procedures that would ensure that interference points
such as the HI-TRAC bottom pool lid did not exist during MPC transfer operations.
The licensee documented the issue in its corrective action program (IR 1109925),
and added procedural guidance.


Analysis:  The inspectors determined that the licensee's failure to have adequate procedures was a violation that warranted a significance evaluation. Consistent with the
                                SUPPLEMENTAL INFORMATION
guidance in Section 2.2 of the NRC Enforcement Policy, ISFSIs are not subject to the
                                  KEY POINTS OF CONTACT
SDP and, thus, traditional enforcement will be used for these facilities. The violation was
Licensee
dispositioned using the traditional enforcement process using Section 2.3 of the  
D. Enright, Site Vice President
Enforcement Policy.  
B. Adams, Plant Manager
L. Bogue, Training Director
The examples were determined to be of more than minor significance because if left
A. Daniels, Nuclear Oversight
uncorrected, these could lead to a more significant safety concern. Consistent with the
C. Gayheart, Operations Director
guidance in Section 2.6.D of the NRC Enforcement Manual, if a violation does not fit an
D. Gudger, Regulatory Assurance Manager
B. Youman, Work Management Director
T. Spelde, ISFSI Project Manager
Nuclear Regulatory Commission
E. Duncan, Chief, Reactor Projects Branch 3
A.M. Stone, Chief, Engineering Branch 3
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
05000454/2010005-01        NCV    Inadequate Instructions for the Inspection of the River
05000455/2010005-01              Screen House and Essential Service Water Cooling Tower
                                  (Section 1R07.1.b)
05000454/2010005-02        NCV    Inadequate Procedures for Implementing FSAR Required
05000455/2010005-02              Annulus Cooling (Section 4OA5.2.b.1)
07200068/2010003-01
05000454/2010005-03        NCV    Inadequate Procedural Guidance for Heavy Loads
05000455/2010005-03              Operations (Section 4OA5.2.b.2)
07200068/2010003-02
Closed
05000454/2010005-01        NCV    Inadequate Instructions for the Inspection of the River
05000455/2010005-01              Screen House and Essential Service Water Cooling Tower
                                  (Section 1R07.1.b)
05000455/2010-001-00      LER    Reactor Protection and Auxiliary Feedwater Actuation
                                  Signals from Low Steam Generator Level Due to Inadequate
                                  Surveillance Testing (Section 4OA3.1)
05000454/2010005-02        NCV    Inadequate Procedures for Implementing FSAR Required
05000455/2010005-02              Annulus Cooling (Section 4OA5.2.b.1)
07200068/2010003-01
05000454/2010005-03        NCV    Inadequate Procedural Guidance for Heavy Loads
05000455/2010005-03              Operations (Section 4OA5.2.b.2)
07200068/2010003-02
                                            1                                Attachment


example in the Enforcement Policy Violation Examples, it should be assigned a severity level: (1) Commensurate with its safety significance; and (2) informed by similar violations addressed in the Violation Examples. The violation screened as having very
                                  LIST OF DOCUMENTS REVIEWED
low safety significance (Severity Level IV).  
The following is a list of documents reviewed during the inspection. Inclusion on this list does
36 Enclosure
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
   Enforcement: 10 CFR 72.150, "Instructions, Procedures, and Drawings," states, in part, that the licensee shall prescribe activities affecting quality by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall require that these instructions, procedures, and drawings be followed.  The instructions, procedures,  
selected sections of portions of the documents were evaluated as part of the overall inspection
and drawings must include appropriate quantitative or qualitative acceptance criteria for
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
determining that important activities have been satisfactorily accomplished.  
any part of it, unless this is stated in the body of the inspection report.
Section 1R01: Adverse Weather Protection
- IR 1130413; Unsecured Items Under 345KV Lines SW of Plant, October 25, 2010
- IR 1131473; TB South Wall Louvers Cannot be Closed, October 27, 2010
- IR 1136634; Antifreeze Not at Correct Concentration 0SX02PB, November 06, 2010
- IR 1138951; Wrong Revision of TB Louver TCCP Installed in Plant, December 01, 2010
- IR 1146976; NOS ID: Winter Readiness Evaluation on TR Tanks, December 01, 2010
- IR 1153775; Winter Readiness Issue - SH Shutdown in January-C&T Level 4,
  December 17, 2010
- IR 1154164; 0BOSR XFT-A1 Freeze Protection Discrepancies, December 19, 2010
- OP-AA-108-111-1001; Severe Weather and Natural Disaster Guidelines, Revision 5
- IR 1122947; NRC Walkdown of ISFSI Storage Pad Area, October 06, 2010
- 0BOSR XFT-A1; Freezing Temperature Equipment Protection SH and Department Support
  Requirements, Rev. 13
- 0BOSR XFT-A3; Freezing Temperature Equipment Protection Plant Ventilation Systems,
  Rev. 7
- 0BOSR XFT-A4; Freezing Temperature Equipment Protection Protected Area Buildings
  Ventilation Systems and Tanks, Rev. 7
- 0BOSR XFT-A5; Freezing Temperature Equipment Protection Non-Protected Area Buildings
   Ventilation Systems, Rev. 5
Section 1R04: Equipment Alignment (Quarterly)
- IR 113291; Review CS009 Concern for Past Reportability, October 27, 2010
- IR 146420; 1B SX Motor Oil Level Too High, November 30, 2010
- IR 146423; 2A SX Motor Oil Level Too High, November 30, 2010
- Drawing M-61; Diagram of Safety Injection, Revision AE
- Drawing M-64; Diagram of Chemical & Volume Control & Boron Thermal Regeneration,
  Revision AY
- IR 1125754; Broken Finder Base Assemblies and Cracked Rotor, October 13, 2010
- IR 1128753; Unplanned LCOAR, 1A CV PP CLR Significant SX Leak, October 20, 2010
- IR 1140870; Normal Valve Position Incorrect on P&ID M-136 SH. 1 - CCP
- BOP CV-1a; Startup of the CV System (Unit 1), Revision 22
- OP-AA-103-102; Watch-Standing Practices, Revision 8
- OP-AA-108-101; Control of Equipment and System Status, Revision 8
- OP-AA-10; Clearance and Tagging Process Description, Revision 2
- M-46; Diagram of Containment Spray, Sheets 1A, 1B, and 1C; Revision AN, AR, and AL
- BOP DG-M1; Diesel Generator System Valve Line-Up, Rev. 19
- BOP DG-21; Diesel Generator Air Receiver Pressure Control, Rev. 5
                                                2                            Attachment


Corrective Action Documents As a Result of NRC Inspection
Contrary to the above, 1. On August 24, 2010, Procedure FH-20; Operation of Fuel Handling Building Crane; Revision 24, was identified to not contain adequate instructions, since the procedure
- IR 1148096; NRC Identified Oil Leak on 2SI8924A Valve, December 2, 2010
failed to establish procedural guidance to instruct crane operators to check holding
- IR 1148603; Clarification Needed for ECCS LCOAR Applicability, December 2, 2010
brakes or define a specific weight as "approaching a rated load."  The licensee documented the issue in its corrective action program.  
- IR 1462222; NRC Concern Being Addressed for SX Oil Reservoir Breather,
2. On September 4, 2010, Procedure BFP FH-69, "HI-TRAC Movement within the Fuel Building," Revision 5, was identified to not contain adequate instruction, since the
  November 30, 2010
procedure failed to have steps in place to ensure the mating device air bags properly deflated and that the HI-TRAC pool lid was correctly positioned on the mating device. The licensee failed to have procedures that would ensure that interference points
Section 1R05: Fire Protection (Quarterly)
such as the HI-TRAC bottom pool lid did not exist during MPC transfer operations.
- Byron Pre-Fire Plan Layout; Unit 2 Auxiliary Building General Area - South-426 Elevation,
   
  Fire Area/Fire Zone: 11.6-0 South
This is a violation of 10 CFR 72.150, "Instructions, Procedures, and Drawings."  This
- Byron Pre-Fire Plan Layout; Auxiliary Building General Area - North-383 Elevation, Fire
Severity Level IV Violation is being treated as a NCV consistent with Section 3.1.1 of the NRC Enforcement Manual.  The licensee documented these issues in its corrective action program as IR1106006 and IR1109925.  (NCV 05000454/2010005-03; 05000455/2010005-03; 07200068/2010003-2, Inadequate Procedural Guidance for Heavy Loads Operations.)
  Area/Fire Zone-11.4-0 North
    4OA6 Meetings
- Byron Pre-Fire Plan Layout; Unit 1 Auxiliary Building 1A Centrifugal Charging Pump Room-
.1 Exit Meeting Summary
  364 Elevation, Fire Area/Fire Zone: 11.3D-1
   On January 13, 2011, the inspectors presented the inspection results to Mr. B. Adams, and other members of the licensee staff.  The licensee personnel acknowledged the
- Byron Pre-Fire Plan Layout; Unit 2 Auxiliary Building General Area - North-364 Elevation, Fire
inspection results presented.  The inspectors confirmed that all proprietary material reviewed during the inspection was returned to the licensee staff. .2 Interim Exit Meetings
  Area/Fire Zone: 11.3-0 North
Interim exits were conducted for:
- Fire Drill 10-04 Minutes; Condensate Polisher Room, December 7, 2010
* The results of the LORT Program inspection with Ms. L. Bogue on October 29, 2010. * The results of the Heat Sink inspection to Mr. B. Adams on December 3, 2010.
- Fire Drill 10-04 Minutes; CP Room, November 30, 2010
* The results of the Radioactive Gaseous and Liquid Effluent Treatment and Performance Indicator Verification inspection with Mr. D. Enright on December 14, 2010. 
- Fire Drill 10-04 Minutes; CP Room, November 23, 2010
37 Enclosure
- OP-AA-201-003; Fire Drill Performance, Revision 11
* The results of the ISFSI Initial Cask Loading Campaign inspection with Mr. D. Enright on December 20, 2010. 
- Byron/Braidwood Fire Protection Report; Section A5.7-20
The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.
  Corrective Action Documents As a Result of NRC Inspection
  ATTACHMENT:  SUPPLEMENTAL INFORMATION    
- IR 1135638; NRC Identified Missing Hardware on 1AP26E, November 04, 2010
1 Attachment  
- IR 1135645; NRC Identified Missing Hardware on 1RY01ED, November 04, 2010
SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT
- IR 1137859; NRC Identified Issue with Conduct of 4th Quarter fire Drills, November 09, 2010
Licensee D. Enright, Site Vice President
- IR 1140585; NRC Identified Degraded Sealant on Concrete Floor Covers, November 15, 2010
Section 1R06: Flood Protection Measures
- IR 648543; Hinge Slade Needs to be Replaced 0DSSD192, July 9, 2007
- IR 878278; MM IR for Weekly and Daily Schedule Adherence, February 2, 2009
- IR 1023213; 0DSSD191 Door Binding in Door Frame, January 29, 2010
Section IR07: Heat Sink
- 0BMSR SX-5, Inspection of River Screen House and Essential Service Water Cooling Tower
   Basins (CM-4), Revision 2
- 0BOL 7.9, LCOAR UHS TS LCO #3.7.9, Revision 12
- IR 1098065, 0BMSR SX-5 Did Not Pass Acceptance Criteria, August 4, 2010
- IR 1111893, Very Minor Leaking, September 9, 2010
- IR 1147407, GL 89-13 HX Acceptance Criteria Still at 10% for some HXs, December 2, 2010
- IR 311626, As-Found Accept Criteria Not Met for 1AF01ABHX; March 11, 2005
- IR 396735, SXCT Fan Gear Box Oil Level W.O. Instructions Need Changing,
  November 8, 2005
- IR 581931, Eddy Current Results on 1A DG Upper Jacket Water Cooler, January 22, 2007
- IR 656533; Replace 10 percent Tube Fouling A.c. w/ design-based for 89-13 HXs,
   August 2, 2007
- IR 865370, Degraded 1A DG JW Cooler Stationary End Divider Plate, January 12, 2009
                                            3                                Attachment


B. Adams, Plant Manager
- BMP 3000-15, Application of Palmer Internationals Tubesheet Cladding System, Revision 1
L. Bogue, Training Director
- BMP 3000-16, Application of Ceramalloy Thin-Film Coating System, Revision 3
A. Daniels, Nuclear Oversight C. Gayheart, Operations Director D. Gudger, Regulatory Assurance Manager
- BOP AF-7T1, Diesel Driven Auxiliary Feedwater Pump Operating Log, Revision 21
B. Youman, Work Management Director
- BOP SX-12, Makeup to an Essential Service Water Mechanical Draft Cooling Tower Basin,
T. Spelde, ISFSI Project Manager
  Revision 9
- BOP SX-13, Initiating and Terminating Essential Service Water System Blowdown, Revision 9
- BOP SX-T2, SX Tower Operation, Revision 14
- BYR 96-277, Determination of Maximum Allowable Silt Depth in River Screen House,
  Devember 10, 1996
- BYR 96-301, Minimum SX Cooling Tower Basin Water Level for Anti-Vortex Duct Flow,
  January 8, 1997
- BYR04-055, Determination of Tube Plugging Limits for DG Jacket Water Coolers,
  September 15, 2010
- CC-AA-309-101, Engineering Technical Evaluations, Revision 11
- EC 339308, Acceptance Criteria for As-Found Heat Exchanger Tube Blockage, Revision 0
- EC 341227, Evaluation Repair of the upper Jacket Water Cooler East Side Divider Plate for
  the 1A Diesel Generator Jacket Water Heat Exchanger, Revision 01
- EC 345255, Acceptance Criteria for As-Found Heat Exchanger Tube Blockage, 1/2AF01AB
  Heat Exchanger, Revision 0
- EC 355109, 1B AF Pump Oil Cooler (1AF01AB) Tube Blockage Evaluation, June 1, 2005
- EC 365231, Establish Tube Plugging Criteria for Eddy Current Testing for 1/2DG01KA/B,
  1/2VP01AA/B/C/D, 0/1/2CC01A, 0WO01C A/B, 1/2VA 01/2/3/4/6S A/B, and 1/2V A08S Heat
  Exchangers
- ER 1147389, Less than adequate Application of EC #355109, December 2, 2010
- ER-AA-340-1002, Service Water Heat Exchanger Inspection Guide, Revision 4
- KSV-20-T, Jacket Water Heat Balance Rev, February 9, 1978
- NDIT BYR97-156, Evaluation of the Ceramalloy Protective to the inlet and floating end
  channels of the DG Jacket Water Coolers per ER9701078
- NED-M-MSD-014, Byron Ultimate Heat Sink Cooling Tower Basin Makeup Calculation,
  April 6, 2008
- NED-Q-MSD-001, ESW Cooling Tower Transient Model: Part I, Revision 0
- SX-TH01, Water Volume in SX System Outdoor Piping and SX Tower Basin, Revision 0
- WO 1050672, EPP GL 89-13 Heat Exchanger Inspection For DG, January 12, 2009
- WO 1218253, Support Diver Insp/Cleaning SXCT South 0B Basin/Sed PM ID 13,
  June 9, 2009
- WO 1232201, SXCT A Cell Inspection Per TRM, May 5, 2010
- WO 1236817, SXCT C Cell Inspection Per TRM, March 3, 2010
- WO 1287340, 1SX01PA Comprehensive IST Req for Essential Service Water Pu,
  February 18, 2010
- WO 1339209, 1SX01PB Comprehensive IST Req for Essential Service Water Pu,
  August 5, 2010
- WO 1342305, Support Diver Insp/Cleaning RSH South 0B Intake/Sed PM ID 30, July 21, 2010
- WO 601958, 1AF01AB - HX Inspection Per Generic Letter 89-13, October 25, 2004
- WO 722875, Exelon Byron Personal Service Report Analytical Report 1B DG Jacket Water
  Deposit Sample, December 18, 2006
- WO 799802, Eddy Current Examination Final Report, January 22, 2010
- WO 840626, EPP GL 89-13 Heat Exchanger Inspection for DG, January 21, 2007
- WO 961095, 1AF 01AB - HX Inspection Per Generic Letter 89-13, February 18, 2008
                                          4                                Attachment


Nuclear Regulatory Commission
Corrective Actions Generated As a Result of the Inspection
E. Duncan, Chief, Reactor Projects Branch 3  
- IR 1142249, Revise Procedure BVP 800-30 to Update Attachment 8, November 18, 2010
A.M. Stone, Chief, Engineering Branch 3  
- IR 1144559, NRC IDD: Work Package Documentation, November 24, 2010
- IR 1144584, NRC IDD: Surveillance Criteria Needs Better Detail, November 24, 2010
- IR 1146808, NRC ID: Enhancement to Rock River Level Monitoring/Silting, December 1, 2010
- IR 1147389, Less Than Adequate Application of EC #355109, December 2, 2010
- IR 1147407, GL 89-13 HX Acceptance Criteria Still at 10% for Some HXs, December 2, 2010
- IR 1147478, NRC Question on SXCT Fan Oil Level Operability, December 2, 2010
Section 1R12: Maintenance Effectiveness
- WO 1206254; Clean Tube Side of Lube Oil Coolers, January 10, 2010
- WO 1387717; Clean Tube Side of Lube Oil Coolers, November 17, 2010
- IR 1141902; 2B DG Upper Lube Oil Hx Check Bolt Torque Tightness, November 17, 2010
- IR 1141905; 2B DG Lower Lube Oil Hx Check Bolt Torque Tightness, November 17, 2010
- IR 1141932; 1A DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010
- IR 1141934; 1A DG Lower Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010
- IR 1141936; 1B DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010
- IR 1141939; 1B DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010
- WO 1387939; Check the Torque on 2B D/G Upper and Lower Lube Oil Cooler,
  November 18, 2010
- WO 1393985; Proof Torque 1B D/G Lower Lube Oil Cooler Stationary Head Bolts,
  December 29, 2010
- WO 1393989; Proof Torque 1B D/G Upper Lube Oil Cooler Stationary Head Bolts,
  December 15, 2010
- WO 1393999; Proof Torque 1A D/G Lower Lube Oil Cooler Stationary Head Bolts,
  January 4, 2011
- WO 1394004; Proof Torque 1A D/G Upper Lube Oil Cooler Stationary Head Bolts,
  December 15, 2011
- List of Run Times for 2A D/G from January to November of 2010
Section 1R13: Maintenance Risk Assessments and Emergent Work Control (Quarterly)
- Draft Risk Assessment for Week of November 29, 2010
- Risk Assessment for Week of November 29, 2010; Revision 1
- Risk Assessment for Week of November 29, 2010; Revision 2
- Risk Assessment for Week of November 29, 2010; Revision 3
- Risk Assessment for Week of November 29, 2010; Revision 4
- Risk Assessment for Week of November 29, 2010; Revision 5
- Risk Assessment for Week of November 29, 2010; Revision 6
- Operations Logs November 29 - December 3, 2010
- WC-AA-101; On-line Work Control Process; Revision 17
- ER-AA-600-1042; On-line Risk Management; Revision 7
Section 1R15: Operability Evaluations (Quarterly)
- IR 709005; 1B Diesel Oil Shows Copper Trending Up - No Threat to Equipment,
  October 07, 2010
- IR 1120751; Pressurizer Steam Space Sample Line Leakage, October 01, 2010
                                            5                              Attachment


- IR 1128756; Unplanned Entry Into 1BOA RCP-12 for #2 Seal Leakoff 1C RCP,
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
  October 20, 2010
Opened 05000454/2010005-01
- IR 1133944; Settings on Woodward Governor, November 02, 2010
05000455/2010005-01 NCV Inadequate Instructions for the Inspection of the River Screen House and Essential Service Water Cooling Tower
- Prompt Investigation; Parts of 7L Piston Pin Bushing Found in Engine Crankcase
(Section 1R07.1.b)
- IR 1112655; Engineering NSRB Subcommittee Observation and Conclusion, September 13,
05000454/2010005-02
  2010
05000455/2010005-02
- IR 1128753; Unplanned LCOAR, 1A CV Pump Cub CLR Significant SX Leak,
07200068/2010003-01 NCV Inadequate Procedures for Implementing FSAR Required Annulus Cooling (Section 4OA5.2.b.1)
  October 20, 2010
- IR 1133944; Settings on Woodward Governor, November 02, 2010
- IR 1149417; Inconsistent SX Piping Configuration for 1B AF PP Lube Oil Cooler,
  December 07, 2010
- Licensee E-Mail from Richard Campbell dated October 26, 2010; Diesel Generator Crank
  Case Oil Copper Trends
- BFP FH-63; Hi-Storm Inspection, Revision 1
- EC 379956; CV Pump Capability with No Cubicle Cooler, August 23, 2010
- Letter from U.S. NRC to Mr. T.E. Herrmann, Chairman, Pressurizer Safety Valve Working
  Group, Westinghouse Owners Group, Subject: Safety Evaluation of Westinghouse Electric
  Corporation Topical Report WCAP - 12910 dated February 19, 1993
- EC 381932; Op Eval 10-005, 2RY8010A Leakage Concerns, Rev. 0
- M-2544A; Unit 1 Essential Service Water Connections for Auxiliary Feedwater , Rev. C
- EC 382473; Op Evaluation 10-008, 1B AF Pump Lube Oil Cooler Piping Wrong,
  December 10, 2010
- IR 1138222; Found FME in the 2A SX Shaft Driven Lube Oil Pump, November 10, 2010
- EC 382534; Evaluation of FME Plug Found in the 2SX01PA Shaft Driven Lube Oil Pump,
  December 14, 2010
Section 1R18: Temporary Modifications
- EC 380566; Temporarily Disconnect Both Sudden Pressure Relays for Main Power
  Transformer 2E Due to Ground Associated with Sudden Pressure Relay 63-1, Rev. 0
- EC 382399; Temporarily Jump Out Cell 42 of ESF Battery 112 to allow 125 VDC ESF Battery
  Operation with 57 Cells, December 3, 2010
- BYR 97-204/BRW-97-0384-E; 125 VDC Battery Sizing Calculation, June 10, 1997
- IEEE STD 485-1983; IEEE Recommended Practice for Sizing Large Lead Storage Batteries
  for Generating Stations and Substations
- BYR97-005-3; C&D Battery Discharge Characteristic Curve, November 18, 1997
Corrective Action Documents As a Result of NRC Inspection
- IR 1123778; NRC Concerns with Timeliness & Pipe Supports, September 30, 2010
Section 1R19: Post Maintenance Testing
- WO 1375300; 1B Diesel Generator Operability Surveillance, October 31, 2010
- WO 1395304; Auctioneer High Tave Function Failed High on Unit 2, December 16, 2010
- IR 1133944; Settings on Woodward Governor, November 2, 2010
- MA-BY-721-061; 125 Volt Battery Bank Quarterly Surveillance, Rev 12
- WO 99070876; Jumper Out Degraded Battery Cell - Battery 112, December 2, 2010
- MA-MW-726-605; 125 Volt DC ESF Battery Cell Jumpering, Rev. 0
                                            6                              Attachment


   05000454/2010005-03
- EC 398100; Verify that NDIT BYR-2001-009, Rev. 0 can be Utilized to meet the Limitation
  Listed in Step 3.2.4 of MA-MW-726-605 for Jumpering Out Cell 42 of Battery 112,
  December 1, 2010
- IR 1146614; 112 Battery Cell 42 Low Cell Voltage, November 30, 2010
Section 1R22: Surveillance Testing
- IR 1122192; GL 08-01 Check-In deficiency - CS full of Water Technical Specifications,
  October 5, 2010
- IR 1122200; GL 08-01 Check-In deficiency - CS Eductor Additive Line, October 5, 2010
- IR 1122268; GL 08-01 Check-In deficiency - BOP CS-5, October 5, 2010
- IR 1122270; GL 08-01 Check-In deficiency - CS NAOH Line, October 5, 2010
- IR 1122272; GL 08-01 Check-In deficiency - CS019 Margin, October 5, 2010
- IR 1131291; Review CS009 Concern for Reportability, October 27, 2010
- IR 1131567; Technical Specifications Bases pH Range Discrepancy, October 27, 2010
- CS System Health Report, Last Updated on June 30, 2010
- IR 1152791; Missing Screw, December 15, 2010
- 2BOSR 6.3.7-1; Unit Two Primary Containment Type C Local Leakage Rate Tests of
  Containment Purge Supply Isolation Valves, Rev. 6
- WO1348943; LLRT for P-97 - 2VQ001A and 2VQ001B, December 15, 2010
Corrective Action Documents As a Result of NRC Inspection
- IR 1159250; NRC Questioned Clearance Between Scaffolds and Unit 2 Containment,
  December 15, 2010
Section 40A1: Performance Indicator Verification
- IR 1094565; SX MSPI Data Discrepancy, July 26, 2010
- IR 1140964; NOS ID Winter Readiness Requirements Not Met, November 16, 2010
- IR 1152376; Unit 2 CWS MSPI Exelon At-Risk, December 14, 2010
Section 40A2: Problem Identification and Resolution
- OP-AA-102-103-1001; 2010 Quarter 4 Assessment, Operator Burden/Degraded Equipment
   Aggregate Assessment, Revision 3
- OP-AA-111-101; Operating Narrative Logs and Records, Revision 7
- Plant Health Committee; Red/Yellow System Action Plan, December 12, 2010
- Letter from HOLTEC International to Exelon Generation Company, LLC, Dated
  November 11, 2010
- SM-AA-102; Warehouse Operations, Revision 14
- Unit 1 & 2 Standing Order; Interim RH Restrictions until Procedures can be Revised,
  December 2, 2010
- Section XI Equipment in Double Frequency, December 14, 2010
- Equipment Important to Emergency Response (EITER) in Degraded Status,
  December 14, 2010
- Equipment Important to Emergency Response (EITER) in Degraded Status Requiring Comp
  Measures, December 14, 2010
- Operator Challenges; December 13, 2010
- Plant Health Committee Agenda, November 29, 2010
- HC Minutes, November 08, 2010
                                            7                                Attachment


05000455/2010005-03
- Issue 1157146; Effectiveness Review of CCA 644073, December 30, 2010
07200068/2010003-02  NCV Inadequate Procedural Guidance for Heavy Loads
- IR 699347; Discrepancy Between Shielding Calculation and Wall Thickness,
Operations (Section 4OA5.2.b.2)
  November 14, 2007
  Closed 05000454/2010005-01
- IR 729631; Apparent Failure to Update Fire Protection Report, January 30, 2008
05000455/2010005-01 NCV Inadequate Instructions for the Inspection of the River Screen House and Essential Service Water Cooling Tower
- IR 723573; Discrepancy in UFSAR Table 3.9-16 Classification, January 17, 2008
(Section 1R07.1.b) 05000455/2010-001-00 LER Reactor Protection and Auxiliary Feedwater Actuation Signals from Low Steam Generator Level Due to Inadequate Surveillance Testing (Section 4OA3.1)
- IR 753012; During 1B AFW Pump Test an Oil Leak Developed with Flames, March 21, 2008
05000454/2010005-02
- IR 761313; BaR15 Coating Inspection Does Not Meet Acceptance Criteria, April 8, 2008
05000455/2010005-02
- IR 765900; Incorrect Emergency Exit Criteria 1BOSR 3.2.8-609D, April 21, 2008
07200068/2010003-01  NCV Inadequate Procedures for Implementing FSAR Required Annulus Cooling (Section 4OA5.2.b.1)
- IR 771208; ECs for Equipment Stored in Containment Due to GSI-191, May 2, 2008
05000454/2010005-03
- IR 773725; Request Documented Clarification of Coating Requirements, May 9, 2008
05000455/2010005-03
- IR 785911; Undocumented SH to WO System Crosstie Pipes found in Auxiliary Building,
07200068/2010003-02  NCV Inadequate Procedural Guidance for Heavy Loads
  June 12, 2008
Operations (Section 4OA5.2.b.2) 
- IR 790335; Need Engineering to Provide Required Reference Dose Rates, June 25, 2008
2 Attachment
- IR 799561; Tube Material Discrepancy in CV and SI Pump Lube Oil Coolers, July 23, 2008
LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection.  Inclusion on this list does
- IR 828275; Tech Spec 4.12 and TRM 5.A Compliance, October 8, 2008
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
Corrective Action Documents As a Result of NRC Inspection
selected sections of portions of the documents were evaluated as part of the overall inspection
- IR 1138034; NRC Discovered Dried Boric Acid on 1FC8762B, November 9, 2010
effort.  Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report. 
- IR 1156959; NRC Questions Aging Engineering, Supply and Operations Actions,
  December 30, 2010
Section 1R01:  Adverse Weather Protection
Section 4OA5: Other Activities
- IR 1130413; Unsecured Items Under 345KV Lines SW of Plant, October 25, 2010 - IR 1131473; TB South Wall Louvers Cannot be Closed, October 27, 2010
- HI-2104725; Vacuum Drying Fuel Temperature Calculation of Byron Cask 1 Under Loss of
- IR 1136634; Antifreeze Not at Correct Concentration 0SX02PB, November 06, 2010
  Annulus Circulation; Revision 0
- IR 1138951; Wrong Revision of TB Louver TCCP Installed in Plant, December 01, 2010 - IR 1146976; NOS ID: Winter Readiness Ev
- IR 1104940; FME - Spent Fuel Pool Cask Pit; August 23, 2010
aluation on TR Tanks, December 01, 2010 - IR 1153775; Winter Readiness Issue - SH Shutdown in January-C&T Level 4, December 17, 2010 - IR 1154164; 0BOSR XFT-A1 Freeze Protection Discrepancies, December 19, 2010
- IR 1105064; Review of Performance on ISFSI FHB / Crane Calculations; August 23, 2010
- OP-AA-108-111-1001; Severe Weather and Natural Disaster Guidelines, Revision 5
- IR 1105388; ISFSI Transporter Failure; August 24, 2010
- IR 1122947; NRC Walkdown of ISFSI Storage Pad Area, October 06, 2010 - 0BOSR XFT-A1; Freezing Temperature Equipment Protection SH and Department Support Requirements, Rev. 13 - 0BOSR XFT-A3; Freezing Temperature Equipment Protection Plant Ventilation Systems, Rev. 7 - 0BOSR XFT-A4; Freezing Temperature Equipment Protection Protected Area Buildings Ventilation Systems and Tanks, Rev. 7 - 0BOSR XFT-A5; Freezing Temperature Equipment Protection Non-Protected Area Buildings Ventilation Systems, Rev. 5 Section 1R04:  Equipment Alignment (Quarterly)
- IR 1105670; South Bridge L/S Stops Crane before Desired Destination; August 25, 2010
- IR 113291; Review CS009 Concern for Past Reportability, October 27, 2010 - IR 146420; 1B SX Motor Oil Level Too High, November 30, 2010
- IR 1105686; Spent Fuel Pit Bridge Crane Delay to Dry Cask Storage; August 25, 2010
- IR 146423; 2A SX Motor Oil Level Too High, November 30, 2010
- IR 1105741; FI-LL, ISFSI Lesson Learned Suggestions, Decon Improvement; August 25, 2010
- Drawing M-61; Diagram of Safety Injection, Revision AE
- IR 1106006; NRC Identifies Procedure Improvements LL; August 26, 2010
- Drawing M-64; Diagram of Chemical & Volume Control & Boron Thermal Regeneration, Revision AY - IR 1125754; Broken Finder Base Assemblies and Cracked Rotor, October 13, 2010
- IR 1106593; NRC ISFSI Inspector 8/26/10 Observations; August 26, 2010
- IR 1128753; Unplanned LCOAR, 1A CV PP CLR Significant SX Leak, October 20, 2010
- IR 1107172; FI-LL, BFP FH-78 for WM CLG Option HI-TRAC Annulus Vacuum Drying System
- IR 1140870; Normal Valve Position Incorrect on P&ID M-136 SH. 1 - CCP
    Operations; August 29, 2010
- BOP CV-1a; Startup of the CV System (Unit 1), Revision 22
- IR 1107675; Holtec FSAR Table 1.2.2 Contains Incorrect Value for MPC 32;
- OP-AA-103-102; Watch-Standing Practices, Revision 8 - OP-AA-108-101; Control of Equipment and System Status, Revision 8 - OP-AA-10; Clearance and Tagging Process Description, Revision 2
    September 29, 2010
- M-46; Diagram of Containment Spray, Sheets 1A, 1B, and 1C; Revision AN, AR, and AL
- IR 1108142; Discrepancy in BFP FH-71; August 31, 2010
- BOP DG-M1; Diesel Generator System Valve Line-Up, Rev. 19
- IR 1108196; SAM #556 Needs Moved Into FHB to Support ISFSI; August 31, 2010
- BOP DG-21; Diesel Generator Air Receiver Pressure Control, Rev. 5
- IR 1108234; Who is in Charge: Exelon Nuclear or Contractors; August 31, 2010
 
- IR 1108255; ISFSI NRC Communications; August 31, 2010
- IR 1108790; Holtec ISFSI Letter on Vacuum Drying was Revised; September 1, 2010
 
- IR 1109916; ISFSI Observations and Lessons Learned; September 4, 2010
3 Attachment
- IR 1109925; Momentary Load Decrease During Multi Purpose Canister Download;
Corrective Action Documents As a Result of NRC Inspection
    September 4, 2010
 
- IR 1110070; ISFSI HI-STORM Transporter Shutdown; September 5, 2010
- IR 1148096; NRC Identified Oil Leak on 2SI8924A Valve, December 2, 2010 - IR 1148603; Clarification Needed for ECCS LCOAR Applicability, December 2, 2010 - IR 1462222; NRC Concern Being Addressed for SX Oil Reservoir Breather, November 30, 2010 Section 1R05: Fire Protection (Quarterly)
- IR 1114568; BWR ISFSI MPCS Require Analysis-Cantera; September 17, 2010
- Byron Pre-Fire Plan Layout; Unit 2 Auxiliary
- IR 1114739; Firewatch Response Requirements need Defined for ISFSI; September 18, 2010
Building General Area - South-426' Elevation, Fire Area/Fire Zone: 11.6-0 South - Byron Pre-Fire Plan Layout; Auxiliary Buildi
- IR 1116408; NRC Potential URIs From ISFSI Reactive Inspection; September 17, 2010
ng General Area - North-383' Elevation, Fire
                                            8                              Attachment
Area/Fire Zone-11.4-0 North - Byron Pre-Fire Plan Layout; Unit 1 Auxiliary
Building 1A Centrifugal Charging Pump Room-364' Elevation, Fire Area/Fire Zone: 11.3D-1 - Byron Pre-Fire Plan Layout; Unit 2 Auxiliary Bu
ilding General Area - North-364' Elevation, Fire
Area/Fire Zone: 11.3-0 North - Fire Drill 10-04 Minutes; Condensate Polisher Room, December 7, 2010  
- Fire Drill 10-04 Minutes; CP Room, November 30, 2010  
- Fire Drill 10-04 Minutes; CP Room, November 23, 2010 - OP-AA-201-003; Fire Drill Performance, Revision 11 - Byron/Braidwood Fire Protection Report; Section A5.7-20
  Corrective Action Documents As a Result of NRC Inspection
  - IR 1135638; NRC Identified Missing Hardware on 1AP26E, November 04, 2010 - IR 1135645; NRC Identified Missing Hardware on 1RY01ED, November 04, 2010  
- IR 1137859; NRC Identified Issue with Conduct of 4
th Quarter fire Drills, November 09, 2010 - IR 1140585; NRC Identified Degraded Sealant on Concrete Floor Covers, November 15, 2010  
Section 1R06:  Flood Protection Measures
- IR 648543; Hinge Slade Needs to be Replaced 0DSSD192, July 9, 2007 - IR 878278; MM IR for Weekly and Daily Schedule Adherence, February 2, 2009 - IR 1023213; 0DSSD191 Door Binding in Door Frame, January 29, 2010  
Section IR07:  Heat Sink
 
- 0BMSR SX-5, Inspection of River Screen House and Essential Service Water Cooling Tower
Basins (CM-4), Revision 2 - 0BOL 7.9, LCOAR UHS TS LCO #3.7.9, Revision 12
- IR 1098065, 0BMSR SX-5 Did Not Pass Acceptance Criteria, August 4, 2010
- IR 1111893, Very Minor Leaking, September 9, 2010 - IR 1147407, GL 89-13 HX Acceptance Criteria Still at 10% for some HX's, December 2, 2010 - IR 311626, As-Found Accept Criteria Not Met for 1AF01ABHX; March 11, 2005
- IR 396735, SXCT Fan Gear Box Oil Level W.O. Instructions Need Changing, November 8, 2005 - IR 581931, Eddy Current Results on 1A DG Upper Jacket Water Cooler, January 22, 2007 - IR 656533; Replace 10 percent Tube Fouling A.c. w/ design-based for 89-13 HX's, August 2, 2007 - IR 865370, Degraded 1A DG JW Cooler Stationary End Divider Plate, January 12, 2009 
4 Attachment
- BMP 3000-15, Application of Palmer International's Tubesheet Cladding System, Revision 1 - BMP 3000-16, Application of Ceramalloy Thin-Film Coating System, Revision 3
- BOP AF-7T1, Diesel Driven Auxiliary Feedwater Pump Operating Log, Revision 21 - BOP SX-12, Makeup to an Essential Service Water Mechanical Draft Cooling Tower Basin, Revision 9 - BOP SX-13, Initiating and Terminating Essential Service Water System Blowdown, Revision 9 - BOP SX-T2, SX Tower Operation, Revision 14
- BYR 96-277, Determination of Maximum Allowable Silt Depth in River Screen House, Devember 10, 1996 - BYR 96-301, Minimum SX Cooling Tower Basin Water Level for Anti-Vortex Duct Flow, January 8, 1997 - BYR04-055, Determination of Tube Plugging Limits for DG Jacket Water Coolers, September 15, 2010 - CC-AA-309-101, Engineering Technical Evaluations, Revision 11 - EC 339308, Acceptance Criteria for As-Found Heat Exchanger Tube Blockage, Revision 0 - EC 341227, Evaluation Repair of the upper Jacket Water Cooler East Side Divider Plate for the 1A Diesel Generator Jacket Water Heat Exchanger, Revision 01 - EC 345255, Acceptance Criteria for As-Found Heat Exchanger Tube Blockage, 1/2AF01AB Heat Exchanger, Revision 0 - EC 355109, 1B AF Pump Oil Cooler (1AF01AB) Tube Blockage Evaluation, June 1, 2005 - EC 365231, Establish Tube Plugging Criteria for Eddy Current Testing for 1/2DG01KA/B, 1/2VP01AA/B/C/D, 0/1/2CC01A, 0WO01C A/B, 1/2VA 01/2/3/4/6S A/B, and 1/2V A08S Heat


Exchangers  - ER 1147389, Less than adequate Application of EC #355109, December 2, 2010
- IR 1119586; Procedure Problems Delay ISFSI Project Startup; September 29, 2010
- ER-AA-340-1002, Service Water Heat Exchanger Inspection Guide, Revision 4 - KSV-20-T, Jacket Water Heat Balance Rev, February 9, 1978 - NDIT BYR97-156, Evaluation of the Ceramalloy Protective to the inlet and floating end channels of the DG Jacket Water Coolers per ER9701078 - NED-M-MSD-014, Byron Ultima
- IR 1121882; FHB Overhead Crane Operating Temperature Outside Procedure;
te Heat Sink Cooling Tower Basin Makeup Calculation, April 6, 2008 - NED-Q-MSD-001, ESW Cooling Tower Transient Model: Part I, Revision 0 - SX-TH01, Water Volume in SX System Outdoor Piping and SX Tower Basin, Revision 0
  October 4, 2010
- WO 1050672, EPP GL 89-13 Heat Exchanger Inspection For DG, January 12, 2009
- IR 1121913; Procedure Changes Needed; October 4, 2010
- WO 1218253, Support Diver Insp/Cleaning SXCT South 0B Basin/Sed PM ID 13, June 9, 2009 - WO 1232201, SXCT A Cell Inspection Per TRM, May 5, 2010 - WO 1236817, SXCT C Cell Inspection Per TRM, March 3, 2010 - WO 1287340, 1SX01PA Comprehensive IST Req for Essential Service Water Pu, February 18, 2010 - WO 1339209, 1SX01PB Comprehensive IST Req for Essential Service Water Pu, August 5, 2010 - WO 1342305, Support Diver Insp/Cleaning RSH South 0B Intake/Sed PM ID 30, July 21, 2010 - WO 601958, 1AF01AB - HX Inspection Per Generic Letter 89-13, October 25, 2004
- IR 1122498; NRC Questioned Items Apparently Stored Near ISFSI Pad; October 5, 2010
- WO 722875, Exelon Byron Personal Service Repor
- IR 1122947; NRC Walkdown of ISFSI Storage Pad Area
t Analytical Report 1B DG Jacket Water
- IR 1123339; FHB Crane Girder Temperature not met Before Use; October 7, 2010
Deposit Sample, December 18, 2006 - WO 799802, Eddy Current Examination Final Report, January 22, 2010
- IR 1123564; ISFSI Mating Device Bolt Stuck
- WO 840626, EPP GL 89-13 Heat Exchanger Inspection for DG, January 21, 2007 
- IR 1124377; Need Temperature Instrument to meet FSAR Requirement; October 9, 2010
- WO 961095, 1AF 01AB - HX Inspection Per Generic Letter 89-13, February 18, 2008
- IR 1125950; ISFSI Procedure Revision for BFP FH-71; October 13, 2010
 
- IR 1126491; ISFSI Bolts Need Evaluation to Establish Criteria; October, 12, 2010
5 Attachment
- IR 1127060; ISFSI Annulus Cooling; October 15, 2010
Corrective Actions Generated As a Result of the Inspection
- IR 1131564; ISFSI Annulus Temperature Analysis; October 27, 2010
  - IR 1142249, Revise Procedure BVP 800-30 to Update Attachment 8, November 18, 2010 - IR 1144559, NRC ID'D: Work Package Documentation, November 24, 2010
- IR 1134848; NSRP Ops Subcommittee - ISFSI IPA Briefing; November 3, 2010
- IR 1144584, NRC ID'D: Surveillance Criteria Needs Better Detail, November 24, 2010 - IR 1146808, NRC ID: Enhancement to Rock River Level Monitoring/Silting, December 1, 2010 - IR 1147389, Less Than Adequate Application of EC #355109, December 2, 2010
- IR 1135839; NOS Identified Issues with ISFSI Related Test Equipment; November 4, 2010
- IR 1147407, GL 89-13 HX Acceptance Criteria Still at 10% for Some HX's, December 2, 2010 - IR 1147478, NRC Question on SXCT Fan Oil Level Operability, December 2, 2010
- IR 1138033; NRC Identified Rust Spots in Vents of HI-STORMS; November 9, 2010
Section 1R12:  Maintenance Effectiveness
- IR 1139597; Continuation of Root Cause Actions for IR 1107151; November 12, 2010
- WO 1206254; Clean Tube Side of Lube Oil Coolers, January 10, 2010 - WO 1387717; Clean Tube Side of Lube Oil Coolers, November 17, 2010
- IR 1139650; ISFSI Fuel Selection Gives Incorrect Max Assembly Enrichment,
- IR 1141902; 2B DG Upper Lube Oil Hx Check Bolt Torque Tightness, November 17, 2010
   November 12, 2010
- IR 1141905; 2B DG Lower Lube Oil Hx Check Bolt Torque Tightness, November 17, 2010 - IR 1141932; 1A DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010 - IR 1141934; 1A DG Lower Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010 - IR 1141936; 1B DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010
- IR 1146205; Engineering Manager needs to Assign 72.212 Coordinator; November 30, 2010
- IR 1141939; 1B DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010
- IR 1146276; Exelon Needs a Common 72.212 Report Change Process; November 30, 2010
- WO 1387939; Check the Torque on 2B D/G Upper and Lower Lube Oil Cooler, November 18, 2010 - WO 1393985; Proof Torque 1B D/G Lower Lube Oil Cooler Stationary Head Bolts, December 29, 2010 - WO 1393989; Proof Torque 1B D/G Upper Lube Oil Cooler Stationary Head Bolts, December 15, 2010 - WO 1393999; Proof Torque 1A D/G Lower Lube Oil Cooler Stationary Head Bolts, January 4, 2011 - WO 1394004; Proof Torque 1A D/G Upper Lube Oil Cooler Stationary Head Bolts, December 15, 2011 - List of Run Times for 2A D/G from January to November of 2010 Section 1R13:  Maintenance Risk Assessments and Emergent Work Control (Quarterly)
- IR 1147090; NRC Identifies Procedure Enhancement; November 24, 2010
- Draft Risk Assessment for Week of November 29, 2010 - Risk Assessment for Week of November 29, 2010; Revision 1
- Risk Assessment for Week of November 29, 2010; Revision 2 - Risk Assessment for Week of November 29, 2010; Revision 3 - Risk Assessment for Week of November 29, 2010; Revision 4
- Risk Assessment for Week of November 29, 2010; Revision 5
- Risk Assessment for Week of November 29, 2010; Revision 6
- Operations Logs November 29 - December 3, 2010
- WC-AA-101; On-line Work Control Process; Revision 17
- ER-AA-600-1042; On-line Risk Management; Revision 7 Section 1R15:  Operability Evaluations (Quarterly)
- IR 709005; 1B Diesel Oil Shows Copper
Trending Up - No Threat to Equipment, October 07, 2010 - IR 1120751; Pressurizer Steam Space Sample Line Leakage, October 01, 2010 
6 Attachment
- IR 1128756; Unplanned Entry Into 1BOA RCP-12 for #2 Seal Leakoff 1C RCP, October 20, 2010 - IR 1133944; Settings on Woodward Governor, November 02, 2010 - Prompt Investigation; Parts of 7L Piston Pin Bushing Found in Engine Crankcase - IR 1112655; Engineering NSRB Subcommittee Observation and Conclusion, September 13, 2010 - IR 1128753; Unplanned LCOAR, 1A CV Pump Cub CLR Significant SX Leak, October 20, 2010 - IR 1133944; Settings on Woodward Governor, November 02, 2010 - IR 1149417; Inconsistent SX Piping Configuration for 1B AF PP Lube Oil Cooler, December 07, 2010 - Licensee E-Mail from Richard Campbell dated October 26, 2010; Diesel Generator Crank
Case Oil Copper Trends - BFP FH-63; Hi-Storm Inspection, Revision 1 - EC 379956; CV Pump Capability with No Cubicle Cooler, August 23, 2010 - Letter from U.S. NRC to Mr. T.E. Herrmann, Chairman, Pressurizer Safety Valve Working Group,  Westinghouse Owners Group, Subject: Safety Evaluation of Westinghouse Electric
Corporation Topical Report WCAP - 12910 dated February 19, 1993 - EC 381932; Op Eval 10-005, 2RY8010A Leakage Concerns, Rev. 0 - M-2544A; Unit 1 Essential Service Water Connections for Auxiliary Feedwater , Rev. C - EC 382473; Op Evaluation 10-008, 1B AF Pump Lube Oil Cooler Piping Wrong, December 10, 2010 - IR 1138222; Found FME in the 2A SX Shaft Driven Lube Oil Pump, November 10, 2010
- EC 382534; Evaluation of FME Plug Found in the 2SX01PA Shaft Driven Lube Oil Pump, December 14, 2010 Section 1R18:  Temporary Modifications
- EC 380566; Temporarily Disconnect Both Sudden Pressure Relays for Main Power Transformer 2E Due to Ground Associated with Sudden Pressure Relay 63-1, Rev. 0 - EC 382399; Temporarily Jump Out Cell 42 of ESF Battery 112 to allow 125 VDC ESF Battery Operation with 57 Cells, December 3, 2010 - BYR 97-204/BRW-97-0384-E; 125 VDC Battery Sizing Calculation, June 10, 1997
- IEEE STD 485-1983; IEEE Recommended Practice for Sizing Large Lead Storage Batteries for Generating Stations and Substations - BYR97-005-3; C&D Battery Discharge Characteristic Curve, November 18, 1997
Corrective Action Documents As a Result of NRC Inspection
  - IR 1123778; NRC Concerns with Timeliness & Pipe Supports, September 30, 2010
Section 1R19:  Post Maintenance Testing
- WO 1375300; 1B Diesel  Generator Operability Surveillance, October 31, 2010 - WO 1395304; Auctioneer High Tave Function Failed High on Unit 2, December 16, 2010
- IR 1133944; Settings on Woodward Governor, November 2, 2010
- MA-BY-721-061; 125 Volt Battery Bank Quarterly Surveillance, Rev 12 - WO 99070876; Jumper Out Degraded Battery Cell - Battery 112, December 2, 2010 - MA-MW-726-605; 125 Volt DC ESF Battery Cell Jumpering, Rev. 0 
7 Attachment
- EC 398100; Verify that NDIT BYR-2001-009, Rev. 0 can be Utilized to meet the Limitation Listed in Step 3.2.4 of MA-MW-726-605 for Jumpering Out Cell 42 of Battery 112,
December 1, 2010 - IR 1146614; 112 Battery Cell 42 Low Cell Voltage, November 30, 2010
Section 1R22:  Surveillance Testing
- IR 1122192; GL 08-01 Check-In deficiency - CS full of Water Technical Specifications, October 5, 2010 - IR 1122200; GL 08-01 Check-In deficiency - CS Eductor Additive Line, October 5, 2010 - IR 1122268; GL 08-01 Check-In deficiency - BOP CS-5, October 5, 2010
- IR 1122270; GL 08-01 Check-In deficiency - CS NAOH Line, October 5, 2010
- IR 1122272; GL 08-01 Check-In deficiency - CS019 Margin, October 5, 2010
- IR 1131291; Review CS009 Concern for Reportability, October 27, 2010 - IR 1131567; Technical Specifications Bases pH Range Discrepancy, October 27, 2010 - CS System Health Report, Last Updated on June 30, 2010
- IR 1152791; Missing Screw, December 15, 2010
- 2BOSR 6.3.7-1; Unit Two Primary Containment Type C Local Leakage Rate Tests of Containment Purge Supply Isolation Valves, Rev. 6 - WO1348943; LLRT for P-97  -  2VQ001A and 2VQ001B, December 15, 2010
Corrective Action Documents As a Result of NRC Inspection
 
- IR 1159250; NRC Questioned Clearance Between Scaffolds and Unit 2 Containment, December 15, 2010 Section 40A1:  Performance Indicator Verification
- IR 1094565; SX MSPI Data Discrepancy, July 26, 2010 - IR 1140964; NOS ID Winter Readiness Requirements Not Met, November 16, 2010 - IR 1152376; Unit 2 CWS MSPI Exelon At-Risk, December 14, 2010 Section 40A2:  Problem Identification and Resolution
- OP-AA-102-103-1001; 2010 Quarter 4 Assessmen
t, Operator Burden/Degraded Equipment Aggregate Assessment, Revision 3 - OP-AA-111-101; Operating Narrative Logs and Records, Revision 7 - Plant Health Committee; Red/Yellow System Action Plan, December 12, 2010
- Letter from HOLTEC International to Exelon Generation Company, LLC, Dated November 11, 2010 - SM-AA-102; Warehouse Operations, Revision 14
- Unit 1 & 2 Standing Order; Interim RH Restrictions until Procedures can be Revised, December 2, 2010 - Section XI Equipment in Double Frequency, December 14, 2010
- Equipment Important to Emergency Response (EITER) in Degraded Status, December 14, 2010 - Equipment Important to Emergency Response (EITER) in Degraded Status Requiring Comp Measures, December 14, 2010 - Operator Challenges; December 13, 2010
- Plant Health Committee Agenda, November 29, 2010
- HC Minutes, November 08, 2010 
8 Attachment
- Issue 1157146; Effectiveness Review of CCA 644073, December 30, 2010 - IR 699347; Discrepancy Between Shielding Calculation and Wall Thickness, November 14, 2007 - IR 729631; Apparent Failure to Update Fire Protection Report, January 30, 2008 - IR 723573; Discrepancy in UFSAR Table 3.9-16 Classification, January 17, 2008
- IR 753012; During 1B AFW Pump Test an Oil Leak Developed with Flames, March 21, 2008
- IR 761313; BaR15 Coating Inspection Does Not Meet Acceptance Criteria, April 8, 2008
- IR 765900; Incorrect Emergency Exit Criteria 1BOSR 3.2.8-609D, April 21, 2008
- IR 771208; EC's for Equipment Stored in Containment Due to GSI-191, May 2, 2008 - IR 773725; Request Documented Clarification of Coating Requirements, May 9, 2008 - IR 785911; Undocumented SH to WO System Crosstie Pipes found in Auxiliary Building, June 12, 2008 - IR 790335; Need Engineering to Provide Required Reference Dose Rates, June 25, 2008
- IR 799561; Tube Material Discrepancy in CV and SI Pump Lube Oil Coolers, July 23, 2008 - IR 828275; Tech Spec 4.12 and TRM 5.A Compliance, October 8, 2008
Corrective Action Documents As a Result of NRC Inspection
  - IR 1138034; NRC Discovered Dried Boric Acid on 1FC8762B, November 9, 2010 - IR 1156959; NRC Questions Aging Engineering, Supply and Operations Actions, December 30, 2010 Section 4OA5:  Other Activities
 
- HI-2104725; Vacuum Drying Fuel Temperature Calculation of Byron Cask 1 Under Loss of Annulus Circulation; Revision 0 - IR 1104940; FME - Spent Fuel Pool Cask Pit; August 23, 2010
- IR 1105064; Review of Performance on ISFSI FHB / Crane Calculations; August 23, 2010 
- IR 1105388; ISFSI Transporter Failure; August 24, 2010  - IR 1105670; South Bridge L/S Stops Crane before Desired Destination; August 25, 2010 - IR 1105686; Spent Fuel Pit Bridge Crane Delay to Dry Cask Storage; August 25, 2010
- IR 1105741; FI-LL, ISFSI Lesson Learned Suggestions, Decon Improvement; August 25, 2010
- IR 1106006; NRC Identifies Procedure Improvements LL; August 26, 2010 - IR 1106593; NRC ISFSI Inspector 8/26/10 Observations; August 26, 2010  - IR 1107172; FI-LL, BFP FH-78 for WM CLG Option HI-TRAC Annulus Vacuum Drying System  Operations; August 29, 2010 - IR 1107675; Holtec FSAR Table 1.2.2 Contains Incorrect Value for MPC 32; 
  September 29, 2010 - IR 1108142; Discrepancy in BFP FH-71; August 31, 2010
- IR 1108196; SAM #556 Needs Moved Into FHB to Support ISFSI; August 31, 2010 - IR 1108234; Who is in Charge: Exelon Nuclear or Contractors; August 31, 2010 - IR 1108255; ISFSI NRC Communications; August 31, 2010
- IR 1108790; Holtec ISFSI Letter on Vacuum Drying was Revised; September 1, 2010
- IR 1109916; ISFSI Observations and Lessons Learned; September 4, 2010
- IR 1109925; Momentary Load Decrease During Multi Purpose Canister Download; 
  September 4, 2010 - IR 1110070; ISFSI HI-STORM Transporter Shutdown; September 5, 2010
- IR 1114568; BWR ISFSI MPCS Require Analysis-Cantera; September 17, 2010
- IR 1114739; Firewatch Response Requirements need Defined for ISFSI; September 18, 2010
- IR 1116408; NRC Potential URIs From ISFSI Reactive Inspection; September 17, 2010 
9 Attachment
- IR 1119586; Procedure Problems Delay ISFSI Project Startup; September 29, 2010 - IR 1121882; FHB Overhead Crane Operating Temperature Outside Procedure;
  October 4, 2010 - IR 1121913; Procedure Changes Needed; October 4, 2010 - IR 1122498; NRC Questioned Items Apparently Stored Near ISFSI Pad; October 5, 2010  
- IR 1122947; NRC Walkdown of ISFSI Storage Pad Area  
- IR 1123339; FHB Crane Girder Temperature not met Before Use; October 7, 2010  
- IR 1123564; ISFSI Mating Device Bolt Stuck  
- IR 1124377; Need Temperature Instrument to meet FSAR Requirement; October 9, 2010 - IR 1125950; ISFSI Procedure Revision for BFP FH-71; October 13, 2010 - IR 1126491; ISFSI Bolts Need Evaluation to Establish Criteria; October, 12, 2010  
- IR 1127060; ISFSI Annulus Cooling; October 15, 2010  
- IR 1131564; ISFSI Annulus Temperature Analysis; October 27, 2010  
- IR 1134848; NSRP Ops Subcommittee - ISFSI IPA Briefing; November 3, 2010 - IR 1135839; NOS Identified Issues with ISFSI Related Test Equipment; November 4, 2010 - IR 1138033; NRC Identified Rust Spots in Vents of HI-STORMS; November 9, 2010  
- IR 1139597; Continuation of Root Cause Actions for IR 1107151; November 12, 2010  
- IR 1139650; ISFSI Fuel Selection Gives Incorrect Max Assembly Enrichment,    November 12, 2010 - IR 1146205; Engineering Manager needs to Assign 72.212 Coordinator; November 30, 2010 - IR 1146276; Exelon Needs a Common 72.212 Report Change Process; November 30, 2010  
- IR 1147090; NRC Identifies Procedure Enhancement; November 24, 2010  
- 72.48-001; 72.212 Evaluation Report Change; Revision 0
- 72.48-001; 72.212 Evaluation Report Change; Revision 0
- 72.48-002; 72.212 Evaluation Report Change 002; Revision 0
- 72.48-002; 72.212 Evaluation Report Change 002; Revision 0
- 72.48-003; HI-TRAC Movement within the Fuel Building; Revision 0
- 72.48-003; HI-TRAC Movement within the Fuel Building; Revision 0
- 72.48-004; Spent Fuel Cask Site Transportation; Revision 0
- 72.48-004; Spent Fuel Cask Site Transportation; Revision 0
- 72.48-005; HI-TRAC Loading Operations; Revision 0
- 72.48-005; HI-TRAC Loading Operations; Revision 0
- 72.48-006; MPC Inspection; Revision 0
- 72.48-006; MPC Inspection; Revision 0
- 72.48-007; Transporter Operations; Revision 0
- 72.48-007; Transporter Operations; Revision 0
- 72.48-008; MPC Alternate Cooling; Revision 0
- 72.48-008; MPC Alternate Cooling; Revision 0
- 72.48-009; MPC Processing; Revision 0
- 72.48-009; MPC Processing; Revision 0
- 72.48-010; Spent Fuel Cask Contingency Actions; Revision 0
- 72.48-010; Spent Fuel Cask Contingency Actions; Revision 0
- 72.48-011; MPC Processing; Revision 0
- 72.48-011; MPC Processing; Revision 0
- 72.48-012; MPC Processing; Revision 0
- 72.48-012; MPC Processing; Revision 0
- 72.48-013; HI-TRTAC Movement within the Fuel Building; Revision 0
- 72.48-013; HI-TRTAC Movement within the Fuel Building; Revision 0
- 72.48-014; HI-TRAC Loading Operations; Revision 0
- 72.48-014; HI-TRAC Loading Operations; Revision 0
- 72.48-015; MPC Alternate Cooling; Revision 0
- 72.48-015; MPC Alternate Cooling; Revision 0
- 72.48-016; Spent Fuel cask Contingency Actions; Revision 0
- 72.48-016; Spent Fuel cask Contingency Actions; Revision 0
- 72.48-017; MPC Processing; Revision 0
- 72.48-017; MPC Processing; Revision 0
- 72.48-018; HI-TRAC Movement within the Fuel Building; Revision 0
- 72.48-018; HI-TRAC Movement within the Fuel Building; Revision 0
- 72.48-019; HI-TRAC Loading Operations; Revision 0
- 72.48-019; HI-TRAC Loading Operations; Revision 0
- 72.48-020; MPC Processing; Revision 0
- 72.48-020; MPC Processing; Revision 0
- 72.48-021; MPC Alternate Cooling; Revision 0
- 72.48-021; MPC Alternate Cooling; Revision 0
- BFP FH-64; Transporter Operations; Revision 4
- BFP FH-64; Transporter Operations; Revision 4
- BFP FH-65; Spent Fuel Cask Site Transportation; Revision 6
- BFP FH-65; Spent Fuel Cask Site Transportation; Revision 6
- BFP FH-68; HI-TRAC Preparation; Revision 2
- BFP FH-68; HI-TRAC Preparation; Revision 2
- BFP FH-69; HI-TRAC Movement within the Fuel Building; Revision 4
- BFP FH-69; HI-TRAC Movement within the Fuel Building; Revision 4
- BFP FH-70; HI-TRAC Loading Operations; Revision 1 - BFP FH-71; MPC Processing; Revision 5
- BFP FH-70; HI-TRAC Loading Operations; Revision 1
- BFP FH-71; MPC Processing; Revision 6
- BFP FH-71; MPC Processing; Revision 5
 
- BFP FH-71; MPC Processing; Revision 6
10 Attachment
                                            9                                Attachment
- BFP FH-71; MPC Processing; Revision 7
 
- BFP FH-71; MPC Processing; Revision 8
- BFP FH-71; MPC Processing; Revision 7
- BFP FH-71; MPC Processing; Revision 9
- BFP FH-71; MPC Processing; Revision 8
- BFP FH-71; MPC Processing; Revision 10
- BFP FH-71; MPC Processing; Revision 9
- BFP FH-71; MPC Processing; Revision 11
- BFP FH-71; MPC Processing; Revision 10
- BFP FH-72; HI-STORM Processing; Revision 0
- BFP FH-71; MPC Processing; Revision 11
- BFP FH-78; Vacuum Drying System Operation; Revision 2
- BFP FH-72; HI-STORM Processing; Revision 0
- BFP Fh-80; Haul Path and ISFSI Dry Run Operations; Revision 0
- BFP FH-78; Vacuum Drying System Operation; Revision 2
- BFP FH-83; Spent Fuel Cask Contingency Actions; Revision 1
- BFP Fh-80; Haul Path and ISFSI Dry Run Operations; Revision 0
- BFP FH-84; HI-TRAC Operations within the Fuel Handling Building; Revision 0
- BFP FH-83; Spent Fuel Cask Contingency Actions; Revision 1
- BFP-FH-20; Operation of Fuel Handling Building Crane; Revision 24
- BFP FH-84; HI-TRAC Operations within the Fuel Handling Building; Revision 0
- LS-BY-105; 72.48 Review Process for Dry Cask Storage; Revision 1
- BFP-FH-20; Operation of Fuel Handling Building Crane; Revision 24
- NF-AP-622; Fuel Selection and Documentation for Dry Cask Storage; Revision 22
- LS-BY-105; 72.48 Review Process for Dry Cask Storage; Revision 1
- Byron Nuclear Power Station, Units 1 and 2; 10 CFR 72.212 Evaluation Report; Revision 0
- NF-AP-622; Fuel Selection and Documentation for Dry Cask Storage; Revision 22
- Holtec Document 1676066; Responses to Potential URIs on Vacuum Drying / Annulus Flush;  
- Byron Nuclear Power Station, Units 1 and 2; 10 CFR 72.212 Evaluation Report; Revision 0
  September 30, 2010
- Holtec Document 1676066; Responses to Potential URIs on Vacuum Drying / Annulus Flush;
- Holtec Document 1676066 R1; Responses to Potential URIs on Vacuum Drying / Annulus   Flush; October 6, 2010
  September 30, 2010
- Apparent Cause Report 1100370; ISFSI Seismic Restraint Bumper Detached from Support  
- Holtec Document 1676066 R1; Responses to Potential URIs on Vacuum Drying / Annulus
Arm - ISFSI Campaign Risk Matrix
  Flush; October 6, 2010
- Root Cause Report 1107151; Annulus Chiller Unit Trip and Associated Organization and  
- Apparent Cause Report 1100370; ISFSI Seismic Restraint Bumper Detached from Support
  Programmatic Issues
  Arm
- 2008 ISFSI Audit Comparative Report; November 6, 2008  
- ISFSI Campaign Risk Matrix
- Root Cause Report 1107151; Annulus Chiller Unit Trip and Associated Organization and
  Programmatic Issues
- 2008 ISFSI Audit Comparative Report; November 6, 2008
- ISFSI Cask Loading Recovery Action Plan; August 30, 2010
- ISFSI Cask Loading Recovery Action Plan; August 30, 2010
- Registration of Use of Cask to Store Spent Fuel ; October 6, 2010
- Registration of Use of Cask to Store Spent Fuel ; October 6, 2010
- Expectation for ISFSI Pad Cleanliness; October 15, 2010
- Expectation for ISFSI Pad Cleanliness; October 15, 2010
- Holtec Document 1678064; VCT Tower Offset; October 22, 2010
- Holtec Document 1678064; VCT Tower Offset; October 22, 2010
- Holtec Document 1678064; Vacuum Drying/Annulus Flush of 21.22 kW MPC; Revision 1
- Holtec Document 1678064; Vacuum Drying/Annulus Flush of 21.22 kW MPC; Revision 1
   
                                            10                          Attachment
11 Attachment
 
LIST OF ACRONYMS USED AC Alternating Current ADAMS Agencywide Document Access Management System ASME American Society of Mechanical Engineers AF Auxiliary Feedwater
                              LIST OF ACRONYMS USED
CAP Corrective Action Program  
AC       Alternating Current
CFR Code of Federal Regulations  
ADAMS   Agencywide Document Access Management System
ºF Degree Fahrenheit  
ASME     American Society of Mechanical Engineers
DC Direct Current EDG Emergency Diesel Generator FHB Fuel Handling Building  
AF       Auxiliary Feedwater
FSAR Final Safety Analysis Report  
CAP     Corrective Action Program
FWIV Feedwater Isolation Valve  
CFR     Code of Federal Regulations
GL Generic Letter HI-STORM Storage Cask HI-TRAC Transfer Cask  
ºF       Degree Fahrenheit
IMC Inspection Manual Chapter  
DC       Direct Current
IP Inspection Procedure  
EDG     Emergency Diesel Generator
IR Issue Report ISFSI Independent Spent Fuel Storage Installation ISG Interim Staff Guidance  
FHB     Fuel Handling Building
JPM Job Performance Measure  
FSAR     Final Safety Analysis Report
LER Licensee Event Report  
FWIV     Feedwater Isolation Valve
LORT Licensed Operator Requalification Training  
GL       Generic Letter
MPC Multi-Purpose Canister MSPI Mitigating Systems Performance Indicator NCV Non-Cited Violation  
HI-STORM Storage Cask
NEI Nuclear Energy Institute  
HI-TRAC Transfer Cask
NRC U.S. Nuclear Regulatory Commission  
IMC     Inspection Manual Chapter
ODCM Occupational Dose Calculation Manual OWA Operator Workaround PARS Publicly Available Records System  
IP       Inspection Procedure
PI Performance Indicator  
IR       Issue Report
RCS Reactor Coolant System  
ISFSI   Independent Spent Fuel Storage Installation
RETS Radiological Effluence Technical Specification
ISG     Interim Staff Guidance
RSH River Screen House SAT Systematic Approach to Training S/G Steam Generator  
JPM     Job Performance Measure
SI Safety Injection  
LER     Licensee Event Report
SPST Spent Fuel Storage and Transportation  
LORT     Licensed Operator Requalification Training
SX Essential Service Water SXCT Essential Service Water Cooling Tower TS Technical Specification  
MPC     Multi-Purpose Canister
UFSAR Updated Final Safety Analysis Report  
MSPI     Mitigating Systems Performance Indicator
USAR Updated Safety Analysis Report UHS Ultimate Heat Sink
NCV     Non-Cited Violation
  M. Pacilio    -2-
NEI     Nuclear Energy Institute
NRC     U.S. Nuclear Regulatory Commission
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the
ODCM     Occupational Dose Calculation Manual
NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's document system (ADAMS). 
OWA     Operator Workaround
ADAMS is accessible from the NRC Website
PARS     Publicly Available Records System
at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). 
PI       Performance Indicator
Sincerely, 
RCS     Reactor Coolant System
/RA/ 
RETS     Radiological Effluence Technical Specification
Eric R. Duncan, Chief
RSH     River Screen House
Branch 3
SAT     Systematic Approach to Training
Division of Reactor Projects
S/G     Steam Generator
  Docket Nos. 50-454; 50-455; 72-068
SI       Safety Injection
License Nos. NPF-37; NPF-66
SPST     Spent Fuel Storage and Transportation
Enclosure: Inspection Report 05000454/2010005; 05000455/2010005; 07200068/2010003  w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ
SX       Essential Service Water
     
SXCT     Essential Service Water Cooling Tower
      DOCUMENT NAME:  G:\DRPIII\BYRO\Byron 2010 005.docx  Publicly Available
TS       Technical Specification
Non-Publicly Available
UFSAR   Updated Final Safety Analysis Report
Sensitive  Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
USAR     Updated Safety Analysis Report
  OFFICE  RIII    RIII        NAME  RNg:dtp  EDuncan    DATE  1/31/11  1/31/11    OFFICIAL RECORD COPY
UHS     Ultimate Heat Sink
 
                                      11                Attachment
  Letter to M. Pacilio from E. Duncan dated January 31, 2011.
  SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT 05000454/2010-005; 05000455/2010-005; 07200068/2010003-2
DISTRIBUTION:
Daniel Merzke
RidsNrrDorlLpl3-2 Resource
RidsNrrPMByron Resource


RidsNrrDirsIrib Resource
M. Pacilio                                                                -2-
Cynthia Pederson
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
Steven Orth Jared Heck
enclosure, and your response (if any) will be available electronically for public inspection in the
Allan Barker
NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website
at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                                          Sincerely,
                                                                          /RA/
                                                                          Eric R. Duncan, Chief
                                                                          Branch 3
                                                                          Division of Reactor Projects
Docket Nos. 50-454; 50-455; 72-068
License Nos. NPF-37; NPF-66
Enclosure:                Inspection Report 05000454/2010005; 05000455/2010005; 07200068/2010003
                            w/Attachment: Supplemental Information
cc w/encl:                Distribution via ListServ
DOCUMENT NAME: G:\DRPIII\BYRO\Byron 2010 005.docx
    Publicly Available                          Non-Publicly Available                    Sensitive                Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE              RIII                                RIII
NAME                RNg:dtp                            EDuncan
DATE                1/31/11                            1/31/11
                                                          OFFICIAL RECORD COPY


Carole Ariano  
Letter to M. Pacilio from E. Duncan dated January 31, 2011.
Linda Linn  
SUBJECT:      BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION
DRPIII  
              REPORT 05000454/2010-005; 05000455/2010-005; 07200068/2010003-2
DRSIII Patricia Buckley Tammy Tomczak  
DISTRIBUTION:
Daniel Merzke
RidsNrrDorlLpl3-2 Resource
RidsNrrPMByron Resource
RidsNrrDirsIrib Resource
Cynthia Pederson
Steven Orth
Jared Heck
Allan Barker
Carole Ariano
Linda Linn
DRPIII
DRSIII
Patricia Buckley
Tammy Tomczak
ROPreports Resource
ROPreports Resource
}}
}}

Latest revision as of 04:04, 13 November 2019

IR 05000454-10-005, 05000455-10-005, 07200068-10-003, on 10/01/10 - 12/31/10, Byron Station, Units 1 & 2, Routine Integrated Inspection Report
ML110310602
Person / Time
Site: Byron  Constellation icon.png
Issue date: 01/31/2011
From: Eric Duncan
Region 3 Branch 3
To: Pacilio M
Exelon Generation Co, Exelon Nuclear
References
IR-10-005
Download: ML110310602 (54)


See also: IR 05000454/2010005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

January 31, 2011

Mr. Michael J. Pacilio

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville IL 60555

SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION

REPORT 05000454/2010-005; 05000455/2010-005; 07200068/2010003-2

Dear Mr. Pacilio:

This refers to the inspection completed on December 31, 2010 at your Byron Station, Units 1

and 2. The enclosed report presents the results of this inspection which were discussed on

January 14, 2011, with Mr. B. Adams, and other members of your staff.

During this inspection, the NRC staff examined activities conducted under your license as they

relate to public health and safety to confirm compliance with the Commission's rules and

regulations and with the conditions of your license. Within these areas, the inspection consisted

of selected examination of procedures and representative records, observations of activities,

and interviews with personnel.

Based on the results of this inspection, the NRC has determined that two Severity Level IV

violations of NRC requirements occurred. The NRC has also identified one issue that was

evaluated under the risk significance determination process as having very low safety

significance (Green). The NRC has determined that one violation is associated with the

issue. These violations are being treated as Non-Cited Violations (NCVs), consistent with

Section 2.3.2 of the Enforcement Policy. These NCVs are described in the subject inspection

report.

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Byron Station. In addition, if you disagree with the cross-cutting aspect assigned to

any finding in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your disagreement, to the Regional Administrator,

Region III, and the NRC Resident Inspector at the Byron Station.

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eric R. Duncan, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454; 50-455;72-068

License Nos. NPF-37; NPF-66

Enclosure: Inspection Report 05000454/2010005; 05000455/2010005; 07200068/2010003

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 05000454; 05000455; 07200068

License Nos: NPF-37; NPF-66

Report No: 05000454/2010005; 05000455/2010005;

07200068/2010003

Licensee: Exelon Generation Company, LLC

Facility: Byron Station, Units 1 and 2

Location: Byron, IL

Dates: October 1, 2010, through December 31, 2010

Inspectors: B. Bartlett, Senior Resident Inspector

J. Robbins, Resident Inspector

M. Bielby, Senior Operations Engineer

R. Edwards, Reactor Engineer

M. Learn, Reactor Engineer

B. Palagi, Senior Operations Engineer

L. Rodriguez, Reactor Engineer

C. Tilton, Senior Reactor Engineer

M. Jones, Reactor Engineer

C. Thompson, Resident Inspector,

Illinois Department of Emergency Management

Approved by: E. Duncan, Chief

Branch 3

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 1

REPORT DETAILS ....................................................................................................................... 3

Summary of Plant Status ........................................................................................................... 3

1. REACTOR SAFETY ....................................................................................................... 3

1R01 Adverse Weather Protection (71111.01) ............................................................. 3

1R04 Equipment Alignment (71111.04) ........................................................................ 4

1R05 Fire Protection (71111.05) ................................................................................... 5

1R06 Flooding (71111.06) ............................................................................................. 7

1R07 Annual Heat Sink Performance (71111.07) ......................................................... 7

1R07 Heat Sink Performance (71111.07T) ................................................................... 8

1R12 Maintenance Effectiveness (71111.12) ............................................................. 15

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ........ 16

1R15 Operability Evaluations (71111.15) .................................................................... 16

1R18 Plant Modifications (71111.18) .......................................................................... 17

1R19 Post Maintenance Testing (71111.19) ............................................................... 18

2. RADIATION SAFETY ................................................................................................... 20

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) .............. 20

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06) ...................... 21

4. OTHER ACTIVITIES (OA) ............................................................................................ 22

4OA1 Performance Indicator Verification (71151) ....................................................... 22

4OA2 Identification and Resolution of Problems (71152) ............................................ 26

4OA3 Followup of Events and Notices of Enforcement Discretion (71153) ................. 28

4OA5 Other Activities ................................................................................................... 29

SUPPLEMENTAL INFORMATION ............................................................................................... 1

KEY POINTS OF CONTACT..................................................................................................... 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 1

LIST OF DOCUMENTS REVIEWED......................................................................................... 2

Enclosure

SUMMARY OF FINDINGS

IR 05000454/2010005, 05000455/2010005; 07200068/2010003; Byron Station, Units 1 & 2;

10/01/10 - 12/31/10; Routine Integrated Inspection Report; Heat Sink Performance; Operation

of an Independent Spent Fuel Storage Installation at Operating Plants

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Severity Level IV Violations and one Green

finding were identified by the inspectors. The Severity Level IV Violations and Green finding

were considered non-cited violations (NCVs) of NRC regulations. The significance of most

findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter

(IMC) 0609, Significance Determination Process (SDP). Assigned cross-cutting aspects were

determined using IMC 0310, Components Within the Cross Cutting Areas. Findings for which

the SDP does not apply may be Green or be assigned a severity level after NRC management

review. The NRCs program for overseeing the safe operation of commercial nuclear power

reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated

December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

  • Green. A finding of very low safety significance and an associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was identified by the inspectors when licensee personnel failed to establish specific

instructions for inspecting the River Screen House and Essential Service Water

Cooling Tower. Specifically, the procedure that provided guidance for inspecting

these structures lacked specific instructions on how to detect concrete degradation,

erosion, corrosion and biological fouling. The licensee entered this issue into their

corrective action program and initiated procedure revisions to provide further

direction for identifying and documenting the degradation of these structures and

related components.

The performance deficiency was determined to be more than minor because if left

uncorrected it would have the potential to lead to a more significant safety concern.

The finding screened as of very low safety significance because it was a qualification

deficiency confirmed not to result in a loss of operability or functionality. Specifically,

a qualitative assessment of historic surveillance reports found the documented

results acceptable. The inspectors determined that this finding did not represent

current licensee performance and therefore no cross-cutting aspect was assigned.

(Section 1R07.1)

Miscellaneous Matters

safety significance of 10 CFR 72.150, "Instruction, Procedures, and Drawings."

Specifically, the licensee failed to have procedures in place to ensure that the design

basis peak fuel cladding limit would not be exceeded during canister loading

1 Enclosure

operations. The licensee entered this issue into their corrective action program and

revised the procedure to provide monitoring criteria.

The violation was determined to be of more than minor significance using IMC 0612,

Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues,

Example 2c, in that the procedures failed to incorporate thermal acceptance criteria

established by the Holtec Final Safety Analysis Report and that the failure to

incorporate thermal acceptance criteria was repetitive. Although the violation

contributed to the likelihood of peak fuel cladding temperatures exceeding the safety

limit, subsequent analysis by the licensee determined that fuel cladding temperature

limits were not exceeded. The violation screened as having very low safety

significance. (Section 4OA5.2)

safety significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings."

Specifically, the licensee failed to have procedures in place to ensure that heavy

loads were operated safely in the Fuel Handling Building. The licensee entered this

issue into their corrective action program and revised the procedure to provide

monitoring criteria.

The violation was determined to be of more than minor significance because if left

uncorrected, it could lead to a more significant safety concern. Consistent with the

guidance in Section 2.6.D of the NRC Enforcement Manual, if a violation does not fit

an example in the Enforcement Policy Violation Examples, it should be assigned a

severity level: (1) commensurate with its safety significance; and (2) informed by

similar violations addressed in the Violation Examples. The violation screened as

having very low safety significance. (Section 4OA5.2)

B. Licensee-Identified Violations

None

2 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full power during the inspection period.

Unit 2 operated at or near full power during the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.2 Winter Seasonal Readiness Preparations

a. Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant specific procedures. Cold weather protection, such as

heat tracing and area heaters, was verified to be in operation where applicable. The

inspectors also reviewed corrective action program (CAP) items to verify that the

licensee was identifying adverse weather issues at an appropriate threshold and

entering them into their CAP in accordance with station corrective action procedures.

Documents reviewed are listed in the Attachment to this report. The inspectors reviews

focused specifically on the following plant systems due to their risk significance or

susceptibility to cold weather issues:

  • Station Heating System (SH);
  • Auxiliary Building Ventilation System (VA); and

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings of significance were identified.

3 Enclosure

.3 Readiness for Impending Adverse Weather Condition - Severe Thunderstorm Watch

and High Wind Conditions

a. Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility on November 22, 2010, and high winds in the area on October 27, 2010,

the inspectors reviewed the licensees overall preparations/protection for the expected

weather conditions. On October 27, 2010, and on November 19, 2010, the inspectors

walked down the plant outside areas, including the main transformers in addition to the

licensees emergency alternating current (AC) power systems, because their

safety-related functions could be affected or required as a result of high winds or

tornado-generated missiles or the loss of offsite power. The inspectors evaluated the

licensee staffs preparations against the sites procedures. During the inspection, the

inspectors focused on plant-specific design features and the licensees procedures used

to respond to specified adverse weather conditions. The inspectors also toured the plant

grounds to look for any loose debris that could become missiles during a tornado. The

inspectors evaluated operator staffing and accessibility of controls and indications for

those systems required to control the plant. Additionally, the inspectors reviewed the

UFSAR and performance requirements for systems selected for inspection, and verified

that operator actions were appropriate as specified by plant specific procedures. The

inspectors also reviewed a sample of CAP items to verify that the licensee identified

adverse weather issues at an appropriate threshold and dispositioned them through the

CAP in accordance with station corrective action procedures. Documents reviewed are

listed in the Attachment to this report.

This inspection constituted two readiness for impending adverse weather condition

samples as defined in IP 71111.01-05.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • Unit 1 Train A Centrifugal Charging and Safety Injection following Maintenance

on the Room Cooler;

Train B Maintenance Outage;

Maintenance Outage;

Service for Planned Maintenance; and

4 Enclosure

  • Unit 2 Train A Safety Injection (SI) while Unit 2 Train B SI was Out of Service for

Planned Maintenance.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders, condition reports, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment.

These activities constituted five partial system walkdown samples as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk significant

plant areas:

  • Auxiliary Building, Electrical Penetration Areas 426' and 414' Elevations (Fire

Zone 11.6-2, 11.5A-2 and 11.5B-2);

  • Auxiliary Building, General Area 426' Elevation (Fire Zone 11.6-0 South);
  • Auxiliary Building, General Area North 364 Elevation (Fire Zone 11.3-0 North);
  • Unit 1 Train A Centrifugal Charging Pump Room (Fire Zone 11.3D-1); and
  • Auxiliary Building, General Area North 383 Elevation (Fire Zone 11.4-0 North).

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan. The

inspectors selected fire areas based on their overall contribution to internal fire risk as

5 Enclosure

documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP. Documents reviewed are

listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings of significance were identified.

.2 Annual Fire Protection Drill Observation (71111.05A)

a. Inspection Scope

On October 20, 2010, the inspectors observed a fire brigade activation for a simulated

fire on the Unit 2 West Main Power Transformer, and on November 30, 2010, the

inspectors observed a portion of a fire brigade activation of a simulated fire in the

Condensate Polisher Room. Based on these observations, the inspectors evaluated the

readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee

staff identified deficiencies; openly discussed them in a self-critical manner at the drill

debrief, and took appropriate corrective actions. Specific attributes evaluated were:

  • proper wearing of turnout gear and self-contained breathing apparatus;
  • proper use and layout of fire hoses;
  • employment of appropriate fire fighting techniques;
  • sufficient firefighting equipment brought to the scene;
  • effectiveness of fire brigade leader communications, command, and control;
  • search for victims and propagation of the fire into other plant areas;
  • smoke removal operations;
  • utilization of pre-planned strategies;
  • adherence to the pre-planned drill scenario; and
  • drill objectives.

Documents reviewed are listed in the Attachment to this report.

These activities constituted two annual fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings of significance were identified.

6 Enclosure

1R06 Flooding (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. Documents reviewed are listed in the Attachment to this

report. In addition, the inspectors reviewed licensee drawings to identify areas and

equipment that may be affected by internal flooding caused by the failure or

misalignment of nearby sources of water, such as the fire suppression or the circulating

water systems. The inspectors also reviewed the licensees corrective action documents

with respect to past flood-related items identified in the corrective action program to

verify the adequacy of the corrective actions. The inspectors performed a walkdown of

the following plant area to assess the adequacy of watertight doors and verify drains and

sumps were clear of debris and were operable, and that the licensee complied with its

commitments:

  • Flood Doors Associated with the Unit 1 Diesel Oil Storage Tank Rooms

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b. Findings

No findings of significance were identified.

1R07 Annual Heat Sink Performance (71111.07)

.1 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the licensees testing of Unit 2 Train A SX Pump Oil Cooler and

Cubicle Coolers to verify that potential deficiencies did not mask the licensees ability to

detect degraded performance, to identify any common cause issues that had the

potential to increase risk, and to ensure that the licensee was adequately addressing

problems that could result in initiating events that would cause an increase in risk. The

inspectors reviewed the licensees observations as compared against acceptance

criteria, the correlation of scheduled testing and the frequency of testing, and the impact

of instrument inaccuracies on test results. The inspectors also verified that test

acceptance criteria considered differences between test conditions, design conditions,

and testing conditions. Documents reviewed are listed in the Attachment to this report.

This annual heat sink performance inspection constituted one sample as defined in

IP 71111.07-05.

7 Enclosure

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07T)

.1 Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed operability determinations, completed surveillances,

vendor manual information, associated calculations, performance test results and

cooler inspection results associated with the 1A EDG jacket water cooler and 1B

auxiliary feed pump oil cooler. These heat exchangers/coolers were chosen based

on their risk-significance in the licensees probabilistic safety analysis, their important

safety-related mitigating system support functions, their operating history, and their

relatively low margin.

For the1A EDG jacket water cooler and the 1B auxiliary feed pump oil cooler the

inspectors verified the methods used to inspect and clean heat exchangers were

consistent with as-found conditions identified and expected degradation trends and

industry standards. The inspectors verified the licensees inspection and cleaning

activities utilized acceptance criteria generated via methods consistent with industry

standards, and that the as-found results were recorded, evaluated, and appropriately

dispositioned. The inspectors also verified that the corrective actions program contained

guidance requiring characterization and evaluation of any foreign materials identified in

the heat exchanger. The inspectors confirmed evaluations were performed to ensure

the heat exchanger would remain capable of performing its intended design function.

The licensee initiated action-tracking items to generate heat exchanger specific tube

plugging and blocking calculations as an enhancement to the heat exchanger monitoring

program for the 1B AF lube oil cooler.

In addition, the inspectors verified the condition and operation of the 1A EDG jacket

water cooler and the 1B AF pump oil cooler were consistent with design assumptions in

heat transfer calculations and Proto HX calculations and as described in the UFSAR.

This included verification that the number of plugged tubes was within pre-established

limits based on capacity and heat transfer assumptions. In addition, eddy current test

reports and visual inspection records were reviewed to determine the structural integrity

of the heat exchanger.

The inspectors verified the performance of ultimate heat sinks (UHSs) and safety-related

service water systems and their subcomponents such as piping, intake screens, pumps,

valves, etc., by tests or other equivalent methods to ensure availability and accessibility

to the in-plant cooling water systems.

The inspectors reviewed the results of the licensees inspection of the UHS and the

River Screen House (RSH). At Byron, the UHS is comprised of the essential service

water cooling tower (SXCT) basin. The inspectors verified that identified settlement or

movement indicating a potential loss of structural integrity was appropriately evaluated

and dispositioned by the licensee. The inspectors also performed walkdowns of

8 Enclosure

accessible portions of components in the SXCT basin to verify the licensees

assessment on structural integrity and component functionality.

The inspectors verified that the licensees inspection of the SXCT basin and the RSH

was comprehensive and of significant depth. The inspectors also verified the licensee

ensured sufficient reservoir capacity by trending and removing debris and sediment

buildup. In addition, the inspectors confirmed that sediments were maintained at an

acceptable level and that water level instruments were functional and routinely

monitored in the UHS. This included the review of the licensees periodic monitoring and

trending of sediment build-up and heat transfer capability calculations.

The inspectors verified the licensees ability to ensure functionality during adverse

weather conditions. The inspectors also verified that the licensee had adequately

protected against silt introduction during periods of low flow or low level.

The inspectors reviewed available licensee testing and inspections results, licensee

disposition of any active thru wall pipe leaks, and the history of thru wall pipe leakage to

identify any adverse trends since the last NRC inspection. For the chemical volume

control system, a closed-cooling system, the inspectors reviewed related documents and

interviewed the system engineer, to identify adverse make-up trends that could be

indicative of excessive leakage out of the closed system. For inaccessible piping, the

inspectors reviewed the licensee's pipe testing, inspection, or monitoring program to

verify structural integrity, and ensured that any leakage or degradation has been

appropriately identified and dispositioned by the licensee. The inspectors verified that

the periodic piping inspection program adequately detected and corrected protective

coating failure, corrosion and erosion. The inspectors verified that the licensee

adequately monitored and resolved any adverse trends for pumps by reviewing the

operational history and in-service testing (IST) vibration monitoring results.

In addition, the inspectors reviewed condition reports related to the heat exchangers and

heat sink performance issues to verify that the licensee had an appropriate threshold for

identifying issues and to evaluate the effectiveness of the corrective actions. Documents

reviewed are listed in the Attachment to this report.

These inspection activities constituted three heat sink inspection samples as defined in

IP 71111.07-05.

b. Findings

(1) Inadequate Instructions for the Inspection of the River Screen House and Essential

Service Water Cooling Tower

Introduction: A finding of very low safety significance (Green) and an associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, was

identified by the inspectors when licensee personnel failed to establish specific

instructions for inspecting the RSH and SXCT. Specifically, the procedure that provided

guidance for inspecting these structures lacked specific instructions on how to detect

concrete degradation, erosion, corrosion and biological fouling.

Description: On November 24, 2010, the inspectors identified that the licensee failed to

establish adequate instructions in surveillance procedures used to inspect the RSH and

SXCT.

9 Enclosure

In response to Generic Letter (GL) 89-13, Service Water Problems Affecting

Safety-Related Equipment, the licensee committed to inspect the RSH and the SXCT

basin to monitor, trend and evaluate any degradation resulting from erosion, corrosion,

silt buildup and biological fouling.

The purpose section of procedure 0BMSR SX-5, Inspection of River Screen House and

Essential Service Water Cooling Tower Basins (CM-4), states: This procedure

provides guidance for inspection of River Screen House (RSH) Intake Structure and the

Essential Service Water Cooling Tower (SXCT) Basins for concrete degradation, silt

buildup, erosion, corrosion, and biological fouling. However, the inspectors noted the

procedure did not include specific guidance on how to accomplish this purpose. For

example, the inspectors noted the procedure contained Step 4.2.3, which required

inspection of the SX makeup pump, but did not provide guidance on how to accomplish

it or what specific sections of the pump and the basins to inspect. In addition, the

procedure did not provide any instructions for what entails degradation of concrete

structures or components by erosion, corrosion and biological fouling mechanisms. In

addition, the procedure did not provide instructions on when or how to document these

types of degradations. The inspectors were concerned that the lack of written

instructions to identify and record the as-found condition of the RSH and the SXCT basin

could result in the licensees inability to properly assess the effect of erosion, corrosion,

biological fouling and concrete degradation on these structures and related components.

As a corrective action, the licensee initiated Issue Report (IR) 1144584 to revise

Procedure 0BMSR SX-5, and provide specific instructions on how to accomplish the

purpose of the procedure. These instructions will include criteria for what to look for and

how and what to document during these inspections related to component and structural

degradation by erosion, corrosion and biological fouling.

Analysis: The inspectors determined that the licensees failure to establish adequate

instructions in surveillance procedures used to inspect the RSH and SXCT was contrary

to the requirements of 10 CFR Part 50, Appendix B, Criterion V, and was a performance

deficiency.

The performance deficiency was determined to be more than minor because if left

uncorrected it would have the potential to lead to a more significant safety concern.

Specifically, since the licensees procedures did not contain instructions to properly

inspect the RSH and SXCT, the potential existed for an unacceptable degradation of

these structures or related components to go undetected affecting essential service

water operability. Inoperable essential service water trains would place the plant at

increased risk for core damage, which would affect the safety of an operating reactor.

The inspectors determined the finding could be evaluated using the Significance

Determination Process (SDP) in accordance with IMC 0609, Significance Determination

Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of

Findings, Table 4a for the Mitigating System Cornerstone. The finding screened as of

very low safety significance (Green) because the finding was a qualification deficiency

confirmed not to result in a loss of operability or functionality. Specifically, the licensee

performed a history review of the surveillance reports and found the documented results

acceptable. A qualitative assessment of the inspections established reasonable

assurance that they did not represent a loss of operability. The inspectors did not have

further concerns.

10 Enclosure

The inspectors determined that this finding did not represent current licensee

performance and therefore no cross-cutting aspect was assigned.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, required, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances.

Contrary to the above, as of November 24, 2010, the licensee did not establish RSH and

SXCT basin surveillance procedural requirements appropriate to the circumstances.

Specifically, procedure 0BMSR SX-5, Inspection of River Screen House and Essential

Service Water Cooling Tower Basins (CM-4), the procedure used to inspect these

structures, was not appropriate for the circumstances. The procedure lacked

instructions on detecting or recording concrete degradation, erosion, corrosion and

biological fouling. Without these instructions, the effect of any degradation on system

operability could not be evaluated. Because this violation was of very low safety

significance and it was entered into the licensees CAP as IR 1144584, this violation is

being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000454/2010005-01; 05000455/2010005-01, Inadequate Instructions for the

Inspection of the River Screen House and Essential Service Water Cooling Tower)

1R11 Licensed Operator Requalification Program (71111.11)

.1 Facility Operating History (71111.11B)

a. Inspection Scope

The inspectors reviewed the plants operating history from October 26 through

October 27, 2010, to identify operating experience that was expected to be addressed

by the Licensed Operator Requalification Training (LORT) program. The inspector

verified that the identified operating experience had been addressed by the facility

licensee in accordance with the stations approved Systems Approach to Training (SAT)

program to satisfy the requirements of 10 CFR 55.59(c). Documents reviewed are listed

in the Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Licensee Requalification Examinations

a. Inspection Scope

The inspectors performed an inspection of the licensees LORT test/examination

program for compliance with the stations SAT program which would satisfy the

requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material

consisted of two operating tests, each containing two dynamic simulator scenarios and

six job performance measures (JPMs). The written examinations reviewed consisted of

two written examinations; each exam contained 30 questions. The inspectors reviewed

the annual requalification operating test and biennial written examination material to

evaluate general quality, construction, and difficulty level. The inspectors assessed the

11 Enclosure

level of examination material duplication from week-to-week during the current year

operating test. The examiners assessed the amount of written examination material

duplication from week-to-week for the written examination administered in 2010. The

inspectors reviewed the methodology for developing the examinations, including the

LORT program 2-year sample plan, probabilistic risk assessment insights, previously

identified operator performance deficiencies, and plant modifications. Documents

reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.3 Licensee Administration of Requalification Examinations

a. Inspection Scope

The inspectors observed the administration of a requalification operating test to

assess the licensees effectiveness in conducting the test to ensure compliance with

10 CRF 55.59(c)(4). The inspectors evaluated the performance of two crews in parallel

with the facility evaluators during two dynamic simulator scenarios and evaluated various

licensed crew members concurrently with facility evaluators during the administration of

several JPMs. The inspectors assessed the facility evaluators ability to determine

adequate crew and individual performance using objective, measurable standards. The

inspectors observed the training staff personnel administer the operating test, including

conducting pre-examination briefings, evaluations of operator performance, and

individual and crew evaluations upon completion of the operating test. The inspectors

evaluated the ability of the simulator to support the examinations. A specific evaluation

of simulator performance was conducted and documented in the section below titled,

Conformance with Simulator Requirements Specified in 10 CFR 55.46. Documents

reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.4 Examination Security

a. Inspection Scope

The inspectors observed and reviewed the licensees overall licensed operator

requalification examination security program related to examination physical security

(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability

and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.

The inspectors also reviewed the facility licensees examination security procedure, any

corrective actions related to past or present examination security problems at the facility,

and the implementation of security and integrity measures (e.g., security agreements,

sampling criteria, bank use, and test item repetition) throughout the examination

process. Documents reviewed are listed in the Attachment to this report.

12 Enclosure

b. Findings

No findings of significance were identified.

.5 Licensee Training Feedback System

a. Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes for

revising and maintaining its LORT Program up to date, including the use of feedback

from plant events and industry experience information. The inspectors reviewed the

licensees quality assurance oversight activities, including licensee training department

self-assessment reports. The inspectors evaluated the licensees ability to assess the

effectiveness of its LORT program and their ability to implement appropriate corrective

actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and

the licensees SAT program. Documents reviewed are listed in the Attachment to this

report.

b. Findings

No findings of significance were identified.

.6 Licensee Remedial Training Program

a. Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial training

conducted since the previous biennial requalification examinations and the training from

the current examination cycle to ensure that they addressed weaknesses in licensed

operator or crew performance identified during training and plant operations. The

inspectors reviewed remedial training procedures and individual remedial training plans.

This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to

the licensees SAT program. Documents reviewed are listed in the Attachment to this

report.

b. Findings

No findings of significance were identified.

.7 Conformance with Operator License Conditions

a. Inspection Scope

The inspectors reviewed the facility and individual operator licensees' conformance with

the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's

program for maintaining active operator licenses and to assess compliance with

10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the

process for tracking on-shift hours for licensed operators and which control room

positions were granted watch-standing credit for maintaining active operator licenses.

The inspectors reviewed the facility licensee's LORT program to assess compliance with

the requalification program requirements as described by 10 CFR 55.59(c). Additionally,

medical records for 10 licensed operators were reviewed for compliance with

13 Enclosure

10 CFR 55.21 and 55.53(i). Documents reviewed are listed in the Attachment to this

report.

b. Findings

No findings of significance were identified.

.8 Conformance with Simulator Requirements Specified in 10 CFR 55.46

a. Inspection Scope

The inspectors assessed the adequacy of the licensees simulation facility (simulator) for

use in operator licensing examinations and for satisfying experience requirements as

prescribed in 10 CFR 55.46, Simulation Facilities. The inspectors also reviewed a

sample of simulator performance test records (i.e., transient tests, malfunction tests,

steady state tests, and core performance tests), simulator discrepancies, and the

process for ensuring continued assurance of simulator fidelity in accordance with

10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy process to

ensure that simulator fidelity was maintained. Open simulator discrepancies were

reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator

actions as well as on nuclear and thermal hydraulic operating characteristics. The

inspectors conducted interviews with members of the licensees simulator staff about the

configuration control process and completed the IP 71111.11, Appendix C, checklist to

evaluate whether or not the licensees plant-referenced simulator was operating

adequately as required by 10 CFR 55.46(c) and (d). Documents reviewed are listed in

the Attachment to this report.

b. Findings

No findings of significance were identified.

.9 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

On October 26 and October 27, 2010, the inspectors observed two crews of licensed

operators in the plants simulator during licensed operator requalification examinations to

verify that operator performance was adequate, evaluators were identifying and

documenting crew performance problems, and training was being conducted in

accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

14 Enclosure

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11-05.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

Connection.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2) or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

No findings of significance were documented in this inspection report. Additional follow-

up and regulatory conclusions are the subject of NRC IR 05000455/2011011.

15 Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • Work Activities during the Week of November 8 Focusing on Unit 2 Train A SX

Outage; and

  • Work Activities during the Week of November 29 for Unit 1 Emergent Direct

Current (DC) Bus 112 Battery Cell Replacement and Planned Unit 2 Safety

Injection Pump work window.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

two samples as defined in IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • Unit 2 Train A Pressurizer Safety Valve Due to Identified but Unexpected Leakby;
  • Unit 2 Train A SX Foreign Material Discovered within the Lube Oil Pump; and

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

16 Enclosure

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and USAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted three samples as defined in IP 71111.15-05.

b. Findings

No findings of significance were identified.

1R18 Plant Modifications (71111.18)

.1 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the following temporary modifications:

  • Unit 2 Temporarily Disconnect Both Sudden Pressure Relays for Main Power

Transformer 2MP01E due to Ground Associated with Relay 63-1; and

  • Unit 1 Battery Bank 112 Installation of Jumper for Degraded Cell.

The inspectors compared the temporary configuration changes and associated

10 CFR 50.59 screening and evaluation information against the design basis, the

UFSAR, and the TS, as applicable, to verify that the modification did not affect the

operability or availability of the affected system(s). The inspectors also compared the

licensees information to operating experience information to ensure that lessons learned

from other utilities had been incorporated into the licensees decision to implement the

temporary modification. The inspectors, as applicable, performed field verifications to

ensure that the modifications were installed as directed; the modifications operated as

expected; modification testing adequately demonstrated continued system operability,

availability, and reliability; and that operation of the modifications did not impact the

operability of any interfacing systems. Lastly, the inspectors discussed the temporary

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how extended operation with the temporary modification in

place could impact overall plant performance. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two temporary modification samples as defined in

IP 71111.18-05.

b. Findings

No findings of significance were identified.

17 Enclosure

1R19 Post Maintenance Testing (71111.19)

.1 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and

functional capability:

  • Unit 1 Train A Chemical Volume Control Pump Room Cooling Fan Following

Motor Replacement;

  • Unit 1 Train B EDG Following Planned Maintenance Work Window;
  • Unit 1 Battery Bank 112 Installation of Jumper for Degraded Cell;
  • Unit 2 Train A Centrifugal Charging Pump Room Cooler Following Maintenance;
  • Unit 2 Train A EDG Room Ventilation Damper Following Replacement; and
  • Unit 2 Circuit Card Controlling Auctioneered High Average Temperature

Selection.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted seven post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings of significance were identified.

18 Enclosure

1R22 Surveillance Testing (71111.22)

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Valves; and

(ASME) Surveillance Meeting IST Program Requirements.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency were

in accordance with TSs, the USAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, ASMEs code, and

reference values were consistent with the system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

19 Enclosure

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one inservice testing sample and one containment isolation

valve inspection sample as defined in IP 71111.22, Sections -02 and -05.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstones: Occupational and Public Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

The inspection activities supplement those documented in Inspection

Report 05000454/2010003; 0500455/2010003, and constitute one complete

sample as defined in IP 71124.01-05.

.1 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors selected several sealed sources from the licensees inventory records

and assessed whether the sources were accounted for and verified to be intact.

The inspectors evaluated whether any transactions, since the last inspection, involving

nationally tracked sources were reported in accordance with 10 CFR 20.2207.

b. Findings

No findings of significance were identified.

.2 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials (nonfuel) stored within spent fuel and other storage

pools. The inspectors assessed whether appropriate controls (i.e., administrative and

physical controls) were in place to preclude inadvertent removal of these materials from

the pool.

b. Findings

No findings of significance were identified.

20 Enclosure

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)

This inspection constituted a partial sample as defined in IP 71124.06-05.

.1 Inspection Planning and Program Reviews (02.01)

Event Report and Effluent Report Reviews

a. Inspection Scope

The inspectors reviewed the radiological effluent release reports issued since the last

inspection to determine if the reports were submitted as required by the Offsite Dose

Calculation Manual/TSs. The inspectors reviewed anomalous results, unexpected

trends, or abnormal releases identified by the licensee for further inspection to determine

if they were evaluated, were entered in the corrective action program, and were

adequately resolved.

b. Findings

No findings of significance were identified.

Offsite Dose Calculation Manual and Updated Final Safety Analysis Report Review

a. Inspection Scope

The inspectors reviewed UFSAR descriptions of the radioactive effluent monitoring

systems, treatment systems, and effluent flow paths so they can be evaluated during

inspection walkdowns.

The inspectors reviewed changes to the Offsite Dose Calculation Manual made by the

licensee since the last inspection against the guidance in NUREG-1301 and 0133, and

Regulatory Guides 1.109, 1.21 and 4.1. When differences were identified, the

inspectors reviewed the technical basis or evaluations of the change during the onsite

inspection, to determine whether they were technically justified and maintain effluent

releases as-low-as-is-reasonably-achievable.

b. Findings

No findings of significance were identified.

Procedures, Special Reports, and Other Documents

a. Inspection Scope

The inspectors reviewed copies of licensee and third party (independent) evaluation

reports of the effluent monitoring program since the last inspection to gather insights into

the licensees program and aid in selecting areas for inspection review (smart sampling).

b. Findings

No findings of significance were identified.

21 Enclosure

4. OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index - Emergency Alternating Current Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Emergency AC Power System performance indicator (PI) for Unit 1 and

Unit 2 for the period from October 1, 2009 through September 30, 2010. To determine

the accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, dated October 2009, was

used. The inspectors reviewed the licensees operator narrative logs, MSPI derivation

reports, issue reports, event reports and NRC Integrated Inspection Reports for the

period of October 1, 2009, through September 30, 2010, to validate the accuracy of the

submittals. The inspectors reviewed the MSPI component risk coefficient to determine if

it had changed by more than 25 percent in value since the previous inspection, and if so,

whether the change was in accordance with applicable NEI guidance. The inspectors

also reviewed the licensees issue report database to determine if any problems had

been identified with the PI data collected or transmitted for this indicator. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI emergency AC power system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Mitigating Systems Performance Index - High Pressure Injection Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - High Pressure Injection

Systems PI for Unit 1 and Unit 2 for the period from October 1, 2009, through

September 30, 2010. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, dated October 2009, was used. The

inspectors reviewed the licensees operator narrative logs, issue reports, MSPI

derivation reports, event reports, and NRC Integrated Inspection Reports for the period

of October 1, 2009, through September 30, 2010, to validate the accuracy of the

submittals. The inspectors reviewed the MSPI component risk coefficient to determine if

it had changed by more than 25 percent in value since the previous inspection, and if so,

whether the change was in accordance with applicable NEI guidance. The inspectors

also reviewed the licensees issue report database to determine if any problems had

been identified with the PI data collected or transmitted for this indicator. Documents

reviewed are listed in the Attachment to this report.

22 Enclosure

This inspection constituted two MSPI high pressure injection system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.3 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for

Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010. To

determine the accuracy of the PI data reported during those periods, PI definitions and

guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, dated October 2009, was used. The inspectors reviewed the

licensees operator narrative logs, issue reports, event reports, MSPI derivation reports,

and NRC Integrated Inspection Reports for the period of October 1, 2009, through

September 30, 2010, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, whether the change

was in accordance with applicable NEI guidance. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

the PI data collected or transmitted for this indicator. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted two MSPI heat removal system samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.4 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal

System PI for Unit 1 and Unit 2, for the period from October 1, 2009, through

September 30, 2010. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, dated October 2009, was used. The

inspectors reviewed the licensees operator narrative logs, issue reports, MSPI

derivation reports, event reports, and NRC Integrated Inspection Reports for the period

of October 1, 2009, through September 30, 2010, to validate the accuracy of the

submittals. The inspectors reviewed the MSPI component risk coefficient to determine if

it had changed by more than 25 percent in value since the previous inspection, and if so,

whether the change was in accordance with applicable NEI guidance. The inspectors

also reviewed the licensees issue report database to determine if any problems had

been identified with the PI data collected or transmitted for this indicator. Documents

reviewed are listed in the Attachment to this report.

23 Enclosure

This inspection constituted two MSPI residual heat removal system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.5 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI

Unit 1 and Unit 2, for the period from October 1, 2009, through September 30, 2010. To

determine the accuracy of the PI data reported during those periods, PI definitions and

guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, dated October 2009, was used. The inspectors reviewed the

licensees operator narrative logs, issue reports, MSPI derivation reports, event reports,

and NRC Integrated Inspection Reports for the period of October 1, 2009 through

September 30, 2010, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, whether the change

was in accordance with applicable NEI guidance. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI cooling water system samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.6 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the Reactor Coolant System (RCS)

Specific Activity PI for the period from July 2009 through September 2010. The

inspectors used PI definitions and guidance contained in the NEI 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, dated October 2009, to

determine the accuracy of the PI data reported during those periods. The inspectors

reviewed the licensees RCS chemistry samples, TS requirements, issue reports, event

reports, and NRC Integrated IRs for the period of July 2009 through September 2010 to

determine if indicator results were accurately reported. Documents reviewed are listed

in the Attachment to this report

This inspection constituted two reactor coolant systems specific activity sample as

defined in IP 71151-05.

24 Enclosure

b. Findings

No findings of significance were identified.

.7 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences PI for the period of July 2009 through September 2010. The inspectors

used PI definitions and guidance contained in the NEI 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, dated October 2009, to determine the

accuracy of the PI data reported during those periods. The inspectors reviewed

electronic dosimetry dose rate and accumulated dose alarm and dose reports and the

dose assignments for any intakes that occurred for selected dates between July 2009

and September 2010 to determine if indicator results were accurately reported. The

inspectors also conducted walk downs of numerous locked high and very high radiation

area entrances to determine the adequacy of the controls in place for these areas.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one occupational radiological occurrences sample as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.8 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent Technical

Specification (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent

Occurrences performance indicator for the period of July 2009 through September 2010.

The inspectors used PI definitions and guidance contained in the NEI 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, dated October 2009, to

determine the accuracy of the PI data reported during those periods. The inspectors

reviewed the licensees issue report database and selected individual reports generated

since this indicator was last reviewed to identify any potential occurrences such as

unmonitored, uncontrolled, or improperly calculated effluent releases that may have

impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the

results of associated offsite dose calculations for selected dates from July 2009 through

September 2010 to determine if indicator results were accurately reported. The

inspectors also reviewed the licensees methods for quantifying gaseous and liquid

effluents and determining effluent dose. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample

as defined in IP 71151-05.

25 Enclosure

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

26 Enclosure

b. Findings

No findings of significance were identified.

.3 Semi Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the 6 month period of June 1, 2010, through

November 30, 2010, although some examples expanded beyond those dates where the

scope of the trend warranted.

The review also included issues documented outside the normal CAP; including major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings of significance were identified.

.4 Annual Sample: Review of Operator Workarounds

a. Inspection Scope

The inspectors evaluated the licensees implementation of their process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the Operator Workarounds

(OWAs) on system availability and the potential for improper operation of the system, for

potential impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents.

The inspectors performed a review of the cumulative effects of OWAs. The documents

listed in the Attachment were reviewed to accomplish the objectives of the inspection

procedure. The inspectors reviewed both current and historical operational challenge

records to determine whether the licensee was identifying operator challenges at an

appropriate threshold, had entered them into their CAP, and proposed or implemented

appropriate and timely corrective actions which addressed each issue. Reviews were

conducted to determine if any operator challenge could increase the possibility of an

initiating event, if the challenge was contrary to training, required a change from

long-standing operational practices, or created the potential for inappropriate

27 Enclosure

compensatory actions. Additionally, all temporary modifications were reviewed to

identify any potential effect on the functionality of Mitigating Systems, impaired access to

equipment, or required equipment uses for which the equipment was not designed.

Daily plant and equipment status logs, degraded instrument logs, and operator aids or

tools being used to compensate for material deficiencies were also assessed to identify

any potential sources of unidentified operator workarounds.

This review constituted one operator workaround annual inspection sample as defined in

IP 71152-05.

b. Findings

No findings of significance were identified.

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000455/2010-001-00: Reactor Protection and

Auxiliary Feedwater Actuation Signals from Low Steam Generator (S/G) Level Due to

Inadequate Surveillance Testing

On April 19, 2010, Unit 2 was in the process of shutting down and cooling down in order

to enter a planned refuelling outage. At 5:03 am with the unit in Mode 4, Hot Shutdown,

a feedwater isolation valve (FWIV) surveillance was in progress and the 2D S/G

secondary side water level lowered to the low S/G water level setpoint, which resulted in

a valid FWIV actuation. All equipment actuated properly and due to the plant condition,

the control rods were already fully inserted with the reactor trip breakers open.

The licensees apparent cause evaluation determined that the operators had received

Just-In-Time training immediately prior to the refuelling outage. However, inadequate

oversight combined with an inadequate procedure had resulted in inadequate control of

the surveillance test activity. The licensee determined that the surveillance procedure

did not allow for S/G levels to be recovered between the testing of the two trains,

performance of the test during the outage was not performed at the optimum time based

on plant parameters, and no pre-job briefing was performed the night of the test. The

licensee had determined that while the test was performed during a time in the outage

that it was usually performed that it had been performed when the RCS was hotter than

it had been before, which resulted in the S/G water level steaming off at a faster rate

than previously experienced.

The inspectors reviewed the Licensee Event Report (LER), licensee procedures, and

performed interviews of selected licensee personnel. The inspectors agreed with the

licensees apparent cause evaluation conclusion regarding the three causes of the FWIV

actuation. The inspectors reviewed the licensees corrective actions and verified that the

corrective actions addressed the causes and were implemented. Corrective actions

included revising the FWIV surveillance procedure, strengthening pre-job briefs, and

reinforcing the roles and responsibilities of key outage operations positions.

Although this issue was corrected, it constituted a performance deficiency and a minor

violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and

Drawings. However, it is not subject to enforcement action in accordance with

Section 2.3.1 of the Enforcement Policy. Because the performance deficiency was not

28 Enclosure

more than minor and not a finding per IMC 0612, Appendix B, Issue Screening, a

cross-cutting aspect was not assigned to this violation.

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA5 Other Activities

.1 Review of Institute of Nuclear Power Operations Report

The inspectors reviewed the Institute of Nuclear Power Operations July 2010 Evaluation

Report, Byron Station, dated December 10, 2010.

.2 Operation of an Independent Spent Fuel Storage Installation at Operating Plants

(60855.1)

a. Inspection Scope

The inspectors observed and evaluated the licensees loading operations of the first and

second multi-purpose canisters (MPC) during the licensees initial spent fuel loading

campaign to verify compliance with the Certificate of Compliance, TS, NRC Regulations,

and associated procedures. The inspectors observed heavy loads movements inside

the Fuel Handling Building (FHB) including: lifting of the transfer cask (HI-TRAC) into the

spent fuel pool, lifting of the HI-TRAC from the spent fuel pool to the decontamination

stand, and transfer of the MPC from the HI-TRAC to the storage cask (HI-STORM) while

the casks are stacked on one another in a laterally restrained configuration. The

inspectors observed loading of spent fuel assemblies from the spent fuel pool into the

MPC. The inspectors observed MPC processing operations including: decontamination

and surveying, canister welding, non-destructive weld examinations, hydrostatic testing,

canister draining, vacuum drying, and helium backfilling. The inspectors observed heavy

loads operations outside of the FHB including: transfer of the HI-STORM from inside of

the FHB to outside of the FHB on a low profile transporter, and transfer of the

HI-STORM to the Independent Spent Fuel Storage Installation (ISFSI) pad using a

vertical cask transporter.

During performance of the activities, the inspectors evaluated the licensee staffs

familiarity with procedures, supervisory oversight, and communication and coordination

between the different groups involved. The inspectors reviewed loading procedures and

evaluated the licensees adherence to these procedures. The inspectors also observed

the licensees process to verify that the contamination and radiation levels from the

transfer cask and storage cask were below the regulatory and TS limits. The inspectors

attended various pre-job briefs to assess the licensees ability to identify critical steps of

the evolution, potential failure scenarios, and tools to prevent errors.

The inspectors reviewed issue reports and the associated follow-up actions that were

generated during the loading campaign as well as 10 CFR 72.48 screenings.

On Saturday, August 28, 2010, the licensees first MPC containing spent nuclear fuel

was left unmonitored during processing operations at the end-of-shift operations. The

MPC had been undergoing vacuum drying throughout the day and at the end of shift

was left under vacuum. While the canister was under vacuum, cooling of the fuel was

significantly reduced, and subsequently fuel temperatures were elevated. The licensees

29 Enclosure

safety analysis for the spent fuel cask system required that the MPC shell temperature

be maintained below 125 degrees Fahrenheit (°F) while the MPC is under vacuum. A

MPC shell temperature of 125°F corresponds to a design basis limit of 1040°F for fuel

cladding temperature as discussed in the Holtec HI-STORM 100 FSAR, Revision 5.

Cooling of the water contained within the HI-TRAC annulus, the area between the MPC

and the HI-TRAC, is provided by a chiller unit when required. For the fuel selected,

annulus cooling would be required to maintain the MPC shell temperature below 125oF.

Prior to the end of shift on August 28, 2010, the inspectors asked the licensee what

plans were in place for monitoring the MPC overnight. The inspectors were informed

that various options were being considered for monitoring the MPC overnight and that a

final decision on the exact method of monitoring and specific staffing had not been

determined. Later that evening, the licensee discussed the importance of the chiller with

technical experts and determined that, due to the heat loads selected for this canister,

heat rates were not high enough to exceed fuel temperature limits even in the event of a

chiller shut off. Therefore, the licensee concluded that no monitoring was necessary

overnight. No specific analysis was performed to support this determination.

On the morning of August 29, 2010, the licensee identified that the chiller had

unexpectedly shut off overnight; however, the licensee failed to recognize that the

annulus water temperature corresponded to a safety limit for fuel cladding temperature

as discussed in the FSAR. A back-up chiller was placed in service promptly; however,

the licensee did not recognize the importance of determining the current water

temperature to ensure that no safety limits were exceeded. The inspectors notified the

licensee of the design basis annulus water temperature limit of 125oF, which was

specified in the FSAR. The inspectors estimated that the 125oF limit was likely

exceeded by several degrees.

The licensee began a prompt evaluation to determine if any fuel cladding safety limits

were exceeded. Working with the licensees vendor, Holtec, the prompt evaluation

concluded that no fuel cladding safety limits were exceeded.

In response to the circumstances of August 28 and 29, 2010, the NRC increased the

oversight of the ISFSI project at the Byron Station and began a reactive inspection on

September 1, 2010. The results of this reactive inspection are documented in NRC

IR Nos. 05000454/2010007; 05000455/2010007; and 07200068/2010002.

Following completion of the reactive inspection the inspectors reviewed the licensees

corrective actions that had been completed and subsequent procedure changes. The

ISFSI inspectors remained onsite for the licensees second MPC loading operations.

Following the second MPC loading, ISFSI inspectors monitored loading operations from

the regional office.

b. Findings

(1) Inadequate Procedures for Implementing Final Safety Analysis Report Required Annulus

Cooling

Introduction: The inspectors identified a Severity Level IV NCV of very low safety

significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings." Specifically,

30 Enclosure

the licensee failed to have procedures in place to ensure that the design basis peak fuel

cladding temperature limit would not be exceeded during canister loading operations.

Description: The licensee revised their ISFSI loading procedures following the

circumstances of August 28 and 29. During review of the revised procedures, the

inspectors identified three examples where the licensee failed to meet the requirements

in 10 CFR 72.150, Instructions, Procedures, and Drawings.

1. Byron Fuel Handling Procedure BFP FH-71, MPC Processing, Revision 8, provides

guidance for the licensee to complete MPC processing operations.

The Holtec FSAR, Revision 5, Chapter 4, discussed how the fuel cladding

temperature limits and associated hoop stress calculation requirements were

consistent with the guidance in Spent Fuel Storage and Transportation (SFST)

Interim Staff Guidance (ISG) - 11 during vacuum drying operations. Specifically, the

Holtec FSAR, Revision 5, Section 4.5.1.1.4.1, Vacuum Drying states, in part:

The initial loading of Spent Nuclear Fuel in the MPC requires that the water

within the MPC be drained and replaced with helium. For MPCs containing

moderate burn-up fuel assemblies only, this operation may be carried out using

the conventional vacuum drying approach. In this method, removal of the last

traces of residual moisture from the MPC cavity is accomplished by evacuating

the MPC for a short time after draining the MPC.

For any decay heat load in an MPC-32, vacuum drying of the MPC is performed

with the annular gap between the MPC and the HI-TRAC continuously flushed

with water. The water movement in this annular gap will maintain the MPC shell

temperature at about the temperature of flowing water. Thus, the thermal

analysis of the MPC during vacuum drying for these conditions is performed with

cooling of the MPC shell with water at a bounding maximum temperature of

125oF.

To avoid excessive conservatism in the computed FLUENT solution, partial

recognition for higher axial heat dissipation is adopted in the peak cladding

calculations. The boundary conditions applied to this evaluation are: ii. The

entire outer surface of the MPC shell is postulated to be at a bounding maximum

temperature of 125°F.

As described in the Holtec FSAR, the intent of flushing water through the annulus

region between the HI-TRAC and the MPC is to maintain the surface of the MPC

shell below 125 °F. The Holtec FSAR states that if MPC shell temperature remains

below 125 °F, the peak fuel cladding temperatures, for moderate burn-up fuel, during

short-term vacuum drying operations, in an MPC with design basis maximum heat

loads, are calculated to be less than the SFST ISG-11 safety limit of 1058ºF.

During vacuum drying operations at the Byron Station, the seal that maintains water

inside the annulus region is removed and allowed to flood several inches over the

top of the MPC. The licensees procedures required the annulus water to be cooled

with a submersible pump, heat exchanger, and chiller. The submersible pump took a

suction of water above the MPC lid and discharged water on the other side of the

31 Enclosure

MPC lid. Temperature measurements were recorded near the suction and discharge

locations. The licensee failed to have an analysis demonstrating that temperatures

measured at the top of the MPC where water was being continuously flushed by a

submersible pump was indicative of canister shell temperatures on the side of the

MPC where water was not being continuously flushed. The licensee failed to

configure the intake and discharge of the submersible pump to ensure that all

regions of the MPC were continuously flushed with water and subsequently failed to

ensure that temperature measurements taken were indicative of the highest shell

temperatures present. The licensee entered these issues into its CAP (IR 1131564)

and initiated actions to evaluate the condition. Following the event, the licensee

contacted the cask vendor, Holtec, and completed an analysis to show that peak fuel

cladding temperature limits were not exceeded. The licensee revised the

configuration of the pump such that the pump intake was at the top of the annulus

and the pump discharge was through the annulus drain line near the bottom of the

annulus.

2. The BFP FH-71, MPC Processing, Revision 8, provides guidance for the licensee

to complete MPC processing operations.

As previously discussed in 4OA5.2.b.1.1, the annulus between the MPC and the

HI-TRAC is required to be continuously flushed with water to ensure that the MPC

shell temperature is maintained below the design basis limit of 125 oF in order to

maintain fuel cladding peak temperatures under design limits as described in the

Holtec FSAR, Revision 5.

The BFP FH-71 contained guidance of when to initiate temperature monitoring of the

annulus region; however the procedure failed to contain guidance of when

temperature monitoring was to be terminated. On October 17, 2010, during MPC

processing operations, the licensee completed vacuum drying operations and

subsequently terminated, without procedural guidance, monitoring of annulus

temperature. At the time monitoring was terminated, the canister was still under

vacuum and annulus temperature requirements were still required by the licensees

design basis. The inspectors brought this discrepancy to the attention of the field

supervisor and the licensee reinitiated temperature monitoring until the MPC was

filled with helium. The licensee entered this issue into in its CAP (IR 1131564) and

completed procedural revisions.

3. The BFP FH-71, MPC Processing, Revision 8, provides guidance for the licensee

to complete MPC processing operations.

On October 15, 2010, an unanalyzed condition was identified regarding spent fuel

peak cladding temperatures while a MPC was filled with nitrogen. The Holtec FSAR

Revision 5 has a thermal analysis for water, helium, and vacuum to exist in the MPC,

however nitrogen, which is used to force water out of the MPC and provide a

temporary inert atmosphere prior to vacuum drying, is unanalyzed. The procedures

section of the Holtec FSAR stated that helium or nitrogen can be used as a gas for

water blowdown operations; however the FSAR did not provide a thermal analysis

for nitrogen. The licensee failed to have an independent thermal analysis for this

condition. The licensee determined that the vacuum thermal analysis bounded the

condition; however this analysis required annulus cooling and imposed MPC shell

32 Enclosure

temperature limits. The licensee initiated annulus cooling, however when the system

actuated, the MPC shell temperature design limit of 125°F was exceeded by several

degrees. Several hours later, the licensee lost function of a chiller in support of

annulus cooling which caused the FSAR temperature limit of 125°F to again be

exceeded for a short period of time. The licensee implemented contingency actions

for the annulus chiller failure, which consisted of a feed of plant demineralized water

into the annulus region and out to plant water treatment to reduce the temperature.

The licensee failed to maintain MPC shell temperatures in accordance with an

associated bounding design basis. The licensee entered this issue into its

corrective action program (IR 1127060). Following the event, the licensee contacted

the cask vendor, Holtec, and completed an analysis to show that peak fuel cladding

temperature limits were not exceeded and initiated procedural changes.

Analysis: The inspectors determined that the licensees failure to have adequate

procedures was a violation that warranted a significance evaluation. Consistent with the

guidance in Section 2.2 of the NRC Enforcement Policy, ISFSIs are not subject to the

SDP and, thus, traditional enforcement will be used for these facilities. The violation was

dispositioned using the traditional enforcement process using Section 2.3 of the

Enforcement Policy.

Example 1 was determined to be of more than minor significance using IMC 0612,

Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues,

Example 3i, in that the licensees lack of evaluation did not assure spent fuel cladding

temperatures during vacuum drying would remain less than SFST ISG-11 safety limits

and an additional calculation was required to evaluate the condition. Examples 2 and 3

were determined to be of more than minor significance using IMC 0612, Power Reactor

Inspection Reports, Appendix E, Examples of Minor Issues, Example 2c, in that the

procedures failed to incorporate thermal acceptance criteria established by the FSAR

and that the failure to incorporate thermal acceptance criteria was repetitive.

Consistent with the guidance in Section 2.6.D of the NRC Enforcement Manual, if a

violation does not fit an example in the Enforcement Policy Violation Examples, it should

be assigned a severity level: (1) commensurate with its safety significance; and

(2) informed by similar violations addressed in the Violation Examples. The inspectors

found no similar violations in the Violation Examples. Subsequent analysis by the

licensee indicated that fuel cladding temperature safety limits were not exceeded;

therefore, the violation was determined to be of very low safety significance (Severity

Level IV).

Enforcement: 10 CFR 72.150, Instructions, Procedures, and Drawings, states, in part,

that the licensee shall prescribe activities affecting quality by documented instructions,

procedures, or drawings of a type appropriate to the circumstances and shall require that

these instructions, procedures, and drawings be followed. The instructions, procedures,

and drawings must include appropriate quantitative or qualitative acceptance criteria for

determining that important activities have been satisfactorily accomplished.

33 Enclosure

Contrary to the above,

1. On October 15, 2010, Procedure BFP FH-71, MPC Processing, Revision 8, was

identified to not contain adequate instructions, since the procedure failed to configure

the intake and discharge of the submersible pump to ensure that all regions of the

MPC were continuously being flushed with water and subsequently failed to ensure

that temperature measurements taken were indicative of the highest MPC shell

temperatures present.

2. On October 15, 2010, Procedure BFP FH-71, MPC Processing, Revision 8, was

identified to not contain adequate instructions, since the procedure failed to contain

guidance of when temperature monitoring was to be terminated. During MPC

processing operations, the licensee completed vacuum drying operations and

subsequently terminated, without procedural guidance, monitoring of annulus

temperatures when annulus temperature requirements were still required by the

licensees design basis.

3. On October 15, 2010, Procedure BFP FH-71, MPC Processing, Revision 8, was

identified to not contain adequate instructions, since the procedure failed to maintain

MPC shell temperatures in accordance with an associated bounding design basis

analysis while the MPC was filled with nitrogen.

This is a violation of 10 CFR 72.150, Instructions, Procedures, and Drawings. This

Severity Level IV Violation is being treated as a NCV consistent with Section 3.1.1 of the

NRC Enforcement Manual. The licensee documented these issues in its corrective

action program as IR 1131564 and IR 1127060. (NCV 05000454/2010005-02;

05000455/2010005-02; 07200068/2010003-1, Inadequate Procedures for

Implementing FSAR Required Annulus Cooling)

(2) Inadequate Procedural Guidance for Heavy Loads Operations

Introduction: The inspectors identified a Severity Level IV NCV of very low safety

significance of 10 CFR 72.150, "Instructions, Procedures, and Drawings." Specifically,

the licensee failed to have procedures in place to ensure that heavy loads were operated

safely in the Fuel Handling Building.

Description: The inspectors identified two examples where the licensee failed to meet

the requirements of 10 CFR 72.150, Instructions, Procedures, and Drawings.

1. On August 24, 2010, the inspectors observed that the crane operator did not check

the hoist brakes on the Fuel Handling Building crane while lifting a HI-TRAC and an

empty MPC from the decontamination stand to the cask wet pit in the spent fuel pool.

The lifted load at the time was approximately 90 tons. The next load to be lifted, a

HI-TRAC with a fully loaded MPC, would be just under the maximum critical load of

the crane, 125 tons.

The Byron Station is committed to following the requirements of ASME B30.2.0-

1976, Overhead and Gantry Cranes (Top Running Bridge, Multiple Girder). In

ASME B30.2.0-1976, Section 2-3.2.3.g, it states The operator shall check the hoist

34 Enclosure

brakes at least once each shift if a load approaching the rated load is to be handled.

This shall be done by raising the load a short distance and applying the brakes.

The inspectors brought the requirements of ASME B30.2.0-1976 to the attention of

the field supervisor and the crane operator checked the crane brakes. The

inspectors reviewed licensee procedures related to heavy loads operations and

determined that no procedural guidance existed to instruct crane operators to check

holding brakes or defined a specific weight as approaching the rated load. The

licensee documented the issue in its corrective action program (IR 1106006), and

added procedural guidance.

2. On September 4, 2010, the licensee was performing MPC transfer operations from

the HI-TRAC to the HI-STORM in a restrained stack configuration using BFP FH-69,

HI-TRAC Movement within the Fuel Building, Revision 5. During withdrawal of the

mating device tongue, the bottom HI-TRAC pool lid became mispositioned in the

mating device when one of the air bags did not fully deflate. The licensee was

unaware this mispositioning placed the edge of the HI-TRAC pool lid in the travel

path of the MPC when it was to be downloaded. The licensee continued and began

to lower the MPC from the HI-TRAC into the HI-STORM. The inspectors observed

that a momentary unexpected load decrease was registered on the Fuel Handling

Building crane load cell from approximately 38 tons to approximately 19 tons. As the

signalman instructed the crane operator to cease lowering, a loud noise was heard,

and the load cell indicated a rapid rise in load back up to approximately 38 tons.

Heavy loads operations were immediately stopped, and plant notifications were

made. The licensee determined that the safest configuration for the MPC would be

inside the HI-STORM and subsequently continued the transfer operation. The

HI-TRAC pool lid had damage to its protective coating. The licensee performed a

walkdown of the crane, inspected the slings for damage, and performed a structural

analysis to show that the MPC could still perform its design function. The licensee

failed to have procedures in place to ensure the mating device air bags properly

deflated and that the HI-TRAC pool lid was correctly positioned on the mating device.

The licensee failed to have procedures that would ensure that interference points

such as the HI-TRAC bottom pool lid did not exist during MPC transfer operations.

The licensee documented the issue in its corrective action program (IR 1109925),

and added procedural guidance.

Analysis: The inspectors determined that the licensees failure to have adequate

procedures was a violation that warranted a significance evaluation. Consistent with the

guidance in Section 2.2 of the NRC Enforcement Policy, ISFSIs are not subject to the

SDP and, thus, traditional enforcement will be used for these facilities. The violation was

dispositioned using the traditional enforcement process using Section 2.3 of the

Enforcement Policy.

The examples were determined to be of more than minor significance because if left

uncorrected, these could lead to a more significant safety concern. Consistent with the

guidance in Section 2.6.D of the NRC Enforcement Manual, if a violation does not fit an

example in the Enforcement Policy Violation Examples, it should be assigned a severity

level: (1) Commensurate with its safety significance; and (2) informed by similar

violations addressed in the Violation Examples. The violation screened as having very

low safety significance (Severity Level IV).

35 Enclosure

Enforcement: 10 CFR 72.150, Instructions, Procedures, and Drawings, states, in part,

that the licensee shall prescribe activities affecting quality by documented instructions,

procedures, or drawings of a type appropriate to the circumstances and shall require that

these instructions, procedures, and drawings be followed. The instructions, procedures,

and drawings must include appropriate quantitative or qualitative acceptance criteria for

determining that important activities have been satisfactorily accomplished.

Contrary to the above,

1. On August 24, 2010, Procedure FH-20; Operation of Fuel Handling Building Crane;

Revision 24, was identified to not contain adequate instructions, since the procedure

failed to establish procedural guidance to instruct crane operators to check holding

brakes or define a specific weight as approaching a rated load. The licensee

documented the issue in its corrective action program.

2. On September 4, 2010, Procedure BFP FH-69, HI-TRAC Movement within the Fuel

Building, Revision 5, was identified to not contain adequate instruction, since the

procedure failed to have steps in place to ensure the mating device air bags properly

deflated and that the HI-TRAC pool lid was correctly positioned on the mating device.

The licensee failed to have procedures that would ensure that interference points

such as the HI-TRAC bottom pool lid did not exist during MPC transfer operations.

This is a violation of 10 CFR 72.150, Instructions, Procedures, and Drawings. This

Severity Level IV Violation is being treated as a NCV consistent with Section 3.1.1 of the

NRC Enforcement Manual. The licensee documented these issues in its corrective

action program as IR1106006 and IR1109925. (NCV 05000454/2010005-03;

05000455/2010005-03; 07200068/2010003-2, Inadequate Procedural Guidance for

Heavy Loads Operations.)

4OA6 Meetings

.1 Exit Meeting Summary

On January 13, 2011, the inspectors presented the inspection results to Mr. B. Adams,

and other members of the licensee staff. The licensee personnel acknowledged the

inspection results presented. The inspectors confirmed that all proprietary material

reviewed during the inspection was returned to the licensee staff.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The results of the LORT Program inspection with Ms. L. Bogue on October 29,

2010.

  • The results of the Heat Sink inspection to Mr. B. Adams on December 3, 2010.
  • The results of the Radioactive Gaseous and Liquid Effluent Treatment and

Performance Indicator Verification inspection with Mr. D. Enright on

December 14, 2010.

36 Enclosure

  • The results of the ISFSI Initial Cask Loading Campaign inspection with

Mr. D. Enright on December 20, 2010.

The licensee acknowledged the issues presented. The inspectors confirmed that none

of the potential report input discussed was considered proprietary.

ATTACHMENT: SUPPLEMENTAL INFORMATION

37 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Enright, Site Vice President

B. Adams, Plant Manager

L. Bogue, Training Director

A. Daniels, Nuclear Oversight

C. Gayheart, Operations Director

D. Gudger, Regulatory Assurance Manager

B. Youman, Work Management Director

T. Spelde, ISFSI Project Manager

Nuclear Regulatory Commission

E. Duncan, Chief, Reactor Projects Branch 3

A.M. Stone, Chief, Engineering Branch 3

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000454/2010005-01 NCV Inadequate Instructions for the Inspection of the River

05000455/2010005-01 Screen House and Essential Service Water Cooling Tower

(Section 1R07.1.b)05000454/2010005-02 NCV Inadequate Procedures for Implementing FSAR Required

05000455/2010005-02 Annulus Cooling (Section 4OA5.2.b.1)

07200068/2010003-01

05000454/2010005-03 NCV Inadequate Procedural Guidance for Heavy Loads05000455/2010005-03 Operations (Section 4OA5.2.b.2)

07200068/2010003-02

Closed

05000454/2010005-01 NCV Inadequate Instructions for the Inspection of the River

05000455/2010005-01 Screen House and Essential Service Water Cooling Tower

(Section 1R07.1.b)

05000455/2010-001-00 LER Reactor Protection and Auxiliary Feedwater Actuation

Signals from Low Steam Generator Level Due to Inadequate

Surveillance Testing (Section 4OA3.1)05000454/2010005-02 NCV Inadequate Procedures for Implementing FSAR Required

05000455/2010005-02 Annulus Cooling (Section 4OA5.2.b.1)

07200068/2010003-01

05000454/2010005-03 NCV Inadequate Procedural Guidance for Heavy Loads05000455/2010005-03 Operations (Section 4OA5.2.b.2)

07200068/2010003-02

1 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

- IR 1130413; Unsecured Items Under 345KV Lines SW of Plant, October 25, 2010

- IR 1131473; TB South Wall Louvers Cannot be Closed, October 27, 2010

- IR 1136634; Antifreeze Not at Correct Concentration 0SX02PB, November 06, 2010

- IR 1138951; Wrong Revision of TB Louver TCCP Installed in Plant, December 01, 2010

- IR 1146976; NOS ID: Winter Readiness Evaluation on TR Tanks, December 01, 2010

- IR 1153775; Winter Readiness Issue - SH Shutdown in January-C&T Level 4,

December 17, 2010

- IR 1154164; 0BOSR XFT-A1 Freeze Protection Discrepancies, December 19, 2010

- OP-AA-108-111-1001; Severe Weather and Natural Disaster Guidelines, Revision 5

- IR 1122947; NRC Walkdown of ISFSI Storage Pad Area, October 06, 2010

- 0BOSR XFT-A1; Freezing Temperature Equipment Protection SH and Department Support

Requirements, Rev. 13

- 0BOSR XFT-A3; Freezing Temperature Equipment Protection Plant Ventilation Systems,

Rev. 7

- 0BOSR XFT-A4; Freezing Temperature Equipment Protection Protected Area Buildings

Ventilation Systems and Tanks, Rev. 7

- 0BOSR XFT-A5; Freezing Temperature Equipment Protection Non-Protected Area Buildings

Ventilation Systems, Rev. 5

Section 1R04: Equipment Alignment (Quarterly)

- IR 113291; Review CS009 Concern for Past Reportability, October 27, 2010

- IR 146420; 1B SX Motor Oil Level Too High, November 30, 2010

- IR 146423; 2A SX Motor Oil Level Too High, November 30, 2010

- Drawing M-61; Diagram of Safety Injection, Revision AE

- Drawing M-64; Diagram of Chemical & Volume Control & Boron Thermal Regeneration,

Revision AY

- IR 1125754; Broken Finder Base Assemblies and Cracked Rotor, October 13, 2010

- IR 1128753; Unplanned LCOAR, 1A CV PP CLR Significant SX Leak, October 20, 2010

- IR 1140870; Normal Valve Position Incorrect on P&ID M-136 SH. 1 - CCP

- BOP CV-1a; Startup of the CV System (Unit 1), Revision 22

- OP-AA-103-102; Watch-Standing Practices, Revision 8

- OP-AA-108-101; Control of Equipment and System Status, Revision 8

- OP-AA-10; Clearance and Tagging Process Description, Revision 2

- M-46; Diagram of Containment Spray, Sheets 1A, 1B, and 1C; Revision AN, AR, and AL

- BOP DG-M1; Diesel Generator System Valve Line-Up, Rev. 19

- BOP DG-21; Diesel Generator Air Receiver Pressure Control, Rev. 5

2 Attachment

Corrective Action Documents As a Result of NRC Inspection

- IR 1148096; NRC Identified Oil Leak on 2SI8924A Valve, December 2, 2010

- IR 1148603; Clarification Needed for ECCS LCOAR Applicability, December 2, 2010

- IR 1462222; NRC Concern Being Addressed for SX Oil Reservoir Breather,

November 30, 2010

Section 1R05: Fire Protection (Quarterly)

- Byron Pre-Fire Plan Layout; Unit 2 Auxiliary Building General Area - South-426 Elevation,

Fire Area/Fire Zone: 11.6-0 South

- Byron Pre-Fire Plan Layout; Auxiliary Building General Area - North-383 Elevation, Fire

Area/Fire Zone-11.4-0 North

- Byron Pre-Fire Plan Layout; Unit 1 Auxiliary Building 1A Centrifugal Charging Pump Room-

364 Elevation, Fire Area/Fire Zone: 11.3D-1

- Byron Pre-Fire Plan Layout; Unit 2 Auxiliary Building General Area - North-364 Elevation, Fire

Area/Fire Zone: 11.3-0 North

- Fire Drill 10-04 Minutes; Condensate Polisher Room, December 7, 2010

- Fire Drill 10-04 Minutes; CP Room, November 30, 2010

- Fire Drill 10-04 Minutes; CP Room, November 23, 2010

- OP-AA-201-003; Fire Drill Performance, Revision 11

- Byron/Braidwood Fire Protection Report; Section A5.7-20

Corrective Action Documents As a Result of NRC Inspection

- IR 1135638; NRC Identified Missing Hardware on 1AP26E, November 04, 2010

- IR 1135645; NRC Identified Missing Hardware on 1RY01ED, November 04, 2010

- IR 1137859; NRC Identified Issue with Conduct of 4th Quarter fire Drills, November 09, 2010

- IR 1140585; NRC Identified Degraded Sealant on Concrete Floor Covers, November 15, 2010

Section 1R06: Flood Protection Measures

- IR 648543; Hinge Slade Needs to be Replaced 0DSSD192, July 9, 2007

- IR 878278; MM IR for Weekly and Daily Schedule Adherence, February 2, 2009

- IR 1023213; 0DSSD191 Door Binding in Door Frame, January 29, 2010

Section IR07: Heat Sink

- 0BMSR SX-5, Inspection of River Screen House and Essential Service Water Cooling Tower

Basins (CM-4), Revision 2

- 0BOL 7.9, LCOAR UHS TS LCO #3.7.9, Revision 12

- IR 1098065, 0BMSR SX-5 Did Not Pass Acceptance Criteria, August 4, 2010

- IR 1111893, Very Minor Leaking, September 9, 2010

- IR 1147407, GL 89-13 HX Acceptance Criteria Still at 10% for some HXs, December 2, 2010

- IR 311626, As-Found Accept Criteria Not Met for 1AF01ABHX; March 11, 2005

- IR 396735, SXCT Fan Gear Box Oil Level W.O. Instructions Need Changing,

November 8, 2005

- IR 581931, Eddy Current Results on 1A DG Upper Jacket Water Cooler, January 22, 2007

- IR 656533; Replace 10 percent Tube Fouling A.c. w/ design-based for 89-13 HXs,

August 2, 2007

- IR 865370, Degraded 1A DG JW Cooler Stationary End Divider Plate, January 12, 2009

3 Attachment

- BMP 3000-15, Application of Palmer Internationals Tubesheet Cladding System, Revision 1

- BMP 3000-16, Application of Ceramalloy Thin-Film Coating System, Revision 3

- BOP AF-7T1, Diesel Driven Auxiliary Feedwater Pump Operating Log, Revision 21

- BOP SX-12, Makeup to an Essential Service Water Mechanical Draft Cooling Tower Basin,

Revision 9

- BOP SX-13, Initiating and Terminating Essential Service Water System Blowdown, Revision 9

- BOP SX-T2, SX Tower Operation, Revision 14

- BYR 96-277, Determination of Maximum Allowable Silt Depth in River Screen House,

Devember 10, 1996

- BYR 96-301, Minimum SX Cooling Tower Basin Water Level for Anti-Vortex Duct Flow,

January 8, 1997

- BYR04-055, Determination of Tube Plugging Limits for DG Jacket Water Coolers,

September 15, 2010

- CC-AA-309-101, Engineering Technical Evaluations, Revision 11

- EC 339308, Acceptance Criteria for As-Found Heat Exchanger Tube Blockage, Revision 0

- EC 341227, Evaluation Repair of the upper Jacket Water Cooler East Side Divider Plate for

the 1A Diesel Generator Jacket Water Heat Exchanger, Revision 01

- EC 345255, Acceptance Criteria for As-Found Heat Exchanger Tube Blockage, 1/2AF01AB

Heat Exchanger, Revision 0

- EC 355109, 1B AF Pump Oil Cooler (1AF01AB) Tube Blockage Evaluation, June 1, 2005

- EC 365231, Establish Tube Plugging Criteria for Eddy Current Testing for 1/2DG01KA/B,

1/2VP01AA/B/C/D, 0/1/2CC01A, 0WO01C A/B, 1/2VA 01/2/3/4/6S A/B, and 1/2V A08S Heat

Exchangers

- ER 1147389, Less than adequate Application of EC #355109, December 2, 2010

- ER-AA-340-1002, Service Water Heat Exchanger Inspection Guide, Revision 4

- KSV-20-T, Jacket Water Heat Balance Rev, February 9, 1978

- NDIT BYR97-156, Evaluation of the Ceramalloy Protective to the inlet and floating end

channels of the DG Jacket Water Coolers per ER9701078

- NED-M-MSD-014, Byron Ultimate Heat Sink Cooling Tower Basin Makeup Calculation,

April 6, 2008

- NED-Q-MSD-001, ESW Cooling Tower Transient Model: Part I, Revision 0

- SX-TH01, Water Volume in SX System Outdoor Piping and SX Tower Basin, Revision 0

- WO 1050672, EPP GL 89-13 Heat Exchanger Inspection For DG, January 12, 2009

- WO 1218253, Support Diver Insp/Cleaning SXCT South 0B Basin/Sed PM ID 13,

June 9, 2009

- WO 1232201, SXCT A Cell Inspection Per TRM, May 5, 2010

- WO 1236817, SXCT C Cell Inspection Per TRM, March 3, 2010

- WO 1287340, 1SX01PA Comprehensive IST Req for Essential Service Water Pu,

February 18, 2010

- WO 1339209, 1SX01PB Comprehensive IST Req for Essential Service Water Pu,

August 5, 2010

- WO 1342305, Support Diver Insp/Cleaning RSH South 0B Intake/Sed PM ID 30, July 21, 2010

- WO 601958, 1AF01AB - HX Inspection Per Generic Letter 89-13, October 25, 2004

- WO 722875, Exelon Byron Personal Service Report Analytical Report 1B DG Jacket Water

Deposit Sample, December 18, 2006

- WO 799802, Eddy Current Examination Final Report, January 22, 2010

- WO 840626, EPP GL 89-13 Heat Exchanger Inspection for DG, January 21, 2007

- WO 961095, 1AF 01AB - HX Inspection Per Generic Letter 89-13, February 18, 2008

4 Attachment

Corrective Actions Generated As a Result of the Inspection

- IR 1142249, Revise Procedure BVP 800-30 to Update Attachment 8, November 18, 2010

- IR 1144559, NRC IDD: Work Package Documentation, November 24, 2010

- IR 1144584, NRC IDD: Surveillance Criteria Needs Better Detail, November 24, 2010

- IR 1146808, NRC ID: Enhancement to Rock River Level Monitoring/Silting, December 1, 2010

- IR 1147389, Less Than Adequate Application of EC #355109, December 2, 2010

- IR 1147407, GL 89-13 HX Acceptance Criteria Still at 10% for Some HXs, December 2, 2010

- IR 1147478, NRC Question on SXCT Fan Oil Level Operability, December 2, 2010

Section 1R12: Maintenance Effectiveness

- WO 1206254; Clean Tube Side of Lube Oil Coolers, January 10, 2010

- WO 1387717; Clean Tube Side of Lube Oil Coolers, November 17, 2010

- IR 1141902; 2B DG Upper Lube Oil Hx Check Bolt Torque Tightness, November 17, 2010

- IR 1141905; 2B DG Lower Lube Oil Hx Check Bolt Torque Tightness, November 17, 2010

- IR 1141932; 1A DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010

- IR 1141934; 1A DG Lower Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010

- IR 1141936; 1B DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010

- IR 1141939; 1B DG Upper Lube Oil Hx Check Bolt Torque Tightness, December 7, 2010

- WO 1387939; Check the Torque on 2B D/G Upper and Lower Lube Oil Cooler,

November 18, 2010

- WO 1393985; Proof Torque 1B D/G Lower Lube Oil Cooler Stationary Head Bolts,

December 29, 2010

- WO 1393989; Proof Torque 1B D/G Upper Lube Oil Cooler Stationary Head Bolts,

December 15, 2010

- WO 1393999; Proof Torque 1A D/G Lower Lube Oil Cooler Stationary Head Bolts,

January 4, 2011

- WO 1394004; Proof Torque 1A D/G Upper Lube Oil Cooler Stationary Head Bolts,

December 15, 2011

- List of Run Times for 2A D/G from January to November of 2010

Section 1R13: Maintenance Risk Assessments and Emergent Work Control (Quarterly)

- Draft Risk Assessment for Week of November 29, 2010

- Risk Assessment for Week of November 29, 2010; Revision 1

- Risk Assessment for Week of November 29, 2010; Revision 2

- Risk Assessment for Week of November 29, 2010; Revision 3

- Risk Assessment for Week of November 29, 2010; Revision 4

- Risk Assessment for Week of November 29, 2010; Revision 5

- Risk Assessment for Week of November 29, 2010; Revision 6

- Operations Logs November 29 - December 3, 2010

- WC-AA-101; On-line Work Control Process; Revision 17

- ER-AA-600-1042; On-line Risk Management; Revision 7

Section 1R15: Operability Evaluations (Quarterly)

- IR 709005; 1B Diesel Oil Shows Copper Trending Up - No Threat to Equipment,

October 07, 2010

- IR 1120751; Pressurizer Steam Space Sample Line Leakage, October 01, 2010

5 Attachment

- IR 1128756; Unplanned Entry Into 1BOA RCP-12 for #2 Seal Leakoff 1C RCP,

October 20, 2010

- IR 1133944; Settings on Woodward Governor, November 02, 2010

- Prompt Investigation; Parts of 7L Piston Pin Bushing Found in Engine Crankcase

- IR 1112655; Engineering NSRB Subcommittee Observation and Conclusion, September 13,

2010

- IR 1128753; Unplanned LCOAR, 1A CV Pump Cub CLR Significant SX Leak,

October 20, 2010

- IR 1133944; Settings on Woodward Governor, November 02, 2010

- IR 1149417; Inconsistent SX Piping Configuration for 1B AF PP Lube Oil Cooler,

December 07, 2010

- Licensee E-Mail from Richard Campbell dated October 26, 2010; Diesel Generator Crank

Case Oil Copper Trends

- BFP FH-63; Hi-Storm Inspection, Revision 1

- EC 379956; CV Pump Capability with No Cubicle Cooler, August 23, 2010

- Letter from U.S. NRC to Mr. T.E. Herrmann, Chairman, Pressurizer Safety Valve Working

Group, Westinghouse Owners Group, Subject: Safety Evaluation of Westinghouse Electric

Corporation Topical Report WCAP - 12910 dated February 19, 1993

- EC 381932; Op Eval 10-005, 2RY8010A Leakage Concerns, Rev. 0

- M-2544A; Unit 1 Essential Service Water Connections for Auxiliary Feedwater , Rev. C

- EC 382473; Op Evaluation 10-008, 1B AF Pump Lube Oil Cooler Piping Wrong,

December 10, 2010

- IR 1138222; Found FME in the 2A SX Shaft Driven Lube Oil Pump, November 10, 2010

- EC 382534; Evaluation of FME Plug Found in the 2SX01PA Shaft Driven Lube Oil Pump,

December 14, 2010

Section 1R18: Temporary Modifications

- EC 380566; Temporarily Disconnect Both Sudden Pressure Relays for Main Power

Transformer 2E Due to Ground Associated with Sudden Pressure Relay 63-1, Rev. 0

- EC 382399; Temporarily Jump Out Cell 42 of ESF Battery 112 to allow 125 VDC ESF Battery

Operation with 57 Cells, December 3, 2010

- BYR 97-204/BRW-97-0384-E; 125 VDC Battery Sizing Calculation, June 10, 1997

- IEEE STD 485-1983; IEEE Recommended Practice for Sizing Large Lead Storage Batteries

for Generating Stations and Substations

- BYR97-005-3; C&D Battery Discharge Characteristic Curve, November 18, 1997

Corrective Action Documents As a Result of NRC Inspection

- IR 1123778; NRC Concerns with Timeliness & Pipe Supports, September 30, 2010

Section 1R19: Post Maintenance Testing

- WO 1375300; 1B Diesel Generator Operability Surveillance, October 31, 2010

- WO 1395304; Auctioneer High Tave Function Failed High on Unit 2, December 16, 2010

- IR 1133944; Settings on Woodward Governor, November 2, 2010

- MA-BY-721-061; 125 Volt Battery Bank Quarterly Surveillance, Rev 12

- WO 99070876; Jumper Out Degraded Battery Cell - Battery 112, December 2, 2010

- MA-MW-726-605; 125 Volt DC ESF Battery Cell Jumpering, Rev. 0

6 Attachment

- EC 398100; Verify that NDIT BYR-2001-009, Rev. 0 can be Utilized to meet the Limitation

Listed in Step 3.2.4 of MA-MW-726-605 for Jumpering Out Cell 42 of Battery 112,

December 1, 2010

- IR 1146614; 112 Battery Cell 42 Low Cell Voltage, November 30, 2010

Section 1R22: Surveillance Testing

- IR 1122192; GL 08-01 Check-In deficiency - CS full of Water Technical Specifications,

October 5, 2010

- IR 1122200; GL 08-01 Check-In deficiency - CS Eductor Additive Line, October 5, 2010

- IR 1122268; GL 08-01 Check-In deficiency - BOP CS-5, October 5, 2010

- IR 1122270; GL 08-01 Check-In deficiency - CS NAOH Line, October 5, 2010

- IR 1122272; GL 08-01 Check-In deficiency - CS019 Margin, October 5, 2010

- IR 1131291; Review CS009 Concern for Reportability, October 27, 2010

- IR 1131567; Technical Specifications Bases pH Range Discrepancy, October 27, 2010

- CS System Health Report, Last Updated on June 30, 2010

- IR 1152791; Missing Screw, December 15, 2010

- 2BOSR 6.3.7-1; Unit Two Primary Containment Type C Local Leakage Rate Tests of

Containment Purge Supply Isolation Valves, Rev. 6

- WO1348943; LLRT for P-97 - 2VQ001A and 2VQ001B, December 15, 2010

Corrective Action Documents As a Result of NRC Inspection

- IR 1159250; NRC Questioned Clearance Between Scaffolds and Unit 2 Containment,

December 15, 2010

Section 40A1: Performance Indicator Verification

- IR 1094565; SX MSPI Data Discrepancy, July 26, 2010

- IR 1140964; NOS ID Winter Readiness Requirements Not Met, November 16, 2010

- IR 1152376; Unit 2 CWS MSPI Exelon At-Risk, December 14, 2010

Section 40A2: Problem Identification and Resolution

- OP-AA-102-103-1001; 2010 Quarter 4 Assessment, Operator Burden/Degraded Equipment

Aggregate Assessment, Revision 3

- OP-AA-111-101; Operating Narrative Logs and Records, Revision 7

- Plant Health Committee; Red/Yellow System Action Plan, December 12, 2010

- Letter from HOLTEC International to Exelon Generation Company, LLC, Dated

November 11, 2010

- SM-AA-102; Warehouse Operations, Revision 14

- Unit 1 & 2 Standing Order; Interim RH Restrictions until Procedures can be Revised,

December 2, 2010

- Section XI Equipment in Double Frequency, December 14, 2010

- Equipment Important to Emergency Response (EITER) in Degraded Status,

December 14, 2010

- Equipment Important to Emergency Response (EITER) in Degraded Status Requiring Comp

Measures, December 14, 2010

- Operator Challenges; December 13, 2010

- Plant Health Committee Agenda, November 29, 2010

- HC Minutes, November 08, 2010

7 Attachment

- Issue 1157146; Effectiveness Review of CCA 644073, December 30, 2010

- IR 699347; Discrepancy Between Shielding Calculation and Wall Thickness,

November 14, 2007

- IR 729631; Apparent Failure to Update Fire Protection Report, January 30, 2008

- IR 723573; Discrepancy in UFSAR Table 3.9-16 Classification, January 17, 2008

- IR 753012; During 1B AFW Pump Test an Oil Leak Developed with Flames, March 21, 2008

- IR 761313; BaR15 Coating Inspection Does Not Meet Acceptance Criteria, April 8, 2008

- IR 765900; Incorrect Emergency Exit Criteria 1BOSR 3.2.8-609D, April 21, 2008

- IR 771208; ECs for Equipment Stored in Containment Due to GSI-191, May 2, 2008

- IR 773725; Request Documented Clarification of Coating Requirements, May 9, 2008

- IR 785911; Undocumented SH to WO System Crosstie Pipes found in Auxiliary Building,

June 12, 2008

- IR 790335; Need Engineering to Provide Required Reference Dose Rates, June 25, 2008

- IR 799561; Tube Material Discrepancy in CV and SI Pump Lube Oil Coolers, July 23, 2008

- IR 828275; Tech Spec 4.12 and TRM 5.A Compliance, October 8, 2008

Corrective Action Documents As a Result of NRC Inspection

- IR 1138034; NRC Discovered Dried Boric Acid on 1FC8762B, November 9, 2010

- IR 1156959; NRC Questions Aging Engineering, Supply and Operations Actions,

December 30, 2010

Section 4OA5: Other Activities

- HI-2104725; Vacuum Drying Fuel Temperature Calculation of Byron Cask 1 Under Loss of

Annulus Circulation; Revision 0

- IR 1104940; FME - Spent Fuel Pool Cask Pit; August 23, 2010

- IR 1105064; Review of Performance on ISFSI FHB / Crane Calculations; August 23, 2010

- IR 1105388; ISFSI Transporter Failure; August 24, 2010

- IR 1105670; South Bridge L/S Stops Crane before Desired Destination; August 25, 2010

- IR 1105686; Spent Fuel Pit Bridge Crane Delay to Dry Cask Storage; August 25, 2010

- IR 1105741; FI-LL, ISFSI Lesson Learned Suggestions, Decon Improvement; August 25, 2010

- IR 1106006; NRC Identifies Procedure Improvements LL; August 26, 2010

- IR 1106593; NRC ISFSI Inspector 8/26/10 Observations; August 26, 2010

- IR 1107172; FI-LL, BFP FH-78 for WM CLG Option HI-TRAC Annulus Vacuum Drying System

Operations; August 29, 2010

- IR 1107675; Holtec FSAR Table 1.2.2 Contains Incorrect Value for MPC 32;

September 29, 2010

- IR 1108142; Discrepancy in BFP FH-71; August 31, 2010

- IR 1108196; SAM #556 Needs Moved Into FHB to Support ISFSI; August 31, 2010

- IR 1108234; Who is in Charge: Exelon Nuclear or Contractors; August 31, 2010

- IR 1108255; ISFSI NRC Communications; August 31, 2010

- IR 1108790; Holtec ISFSI Letter on Vacuum Drying was Revised; September 1, 2010

- IR 1109916; ISFSI Observations and Lessons Learned; September 4, 2010

- IR 1109925; Momentary Load Decrease During Multi Purpose Canister Download;

September 4, 2010

- IR 1110070; ISFSI HI-STORM Transporter Shutdown; September 5, 2010

- IR 1114568; BWR ISFSI MPCS Require Analysis-Cantera; September 17, 2010

- IR 1114739; Firewatch Response Requirements need Defined for ISFSI; September 18, 2010

- IR 1116408; NRC Potential URIs From ISFSI Reactive Inspection; September 17, 2010

8 Attachment

- IR 1119586; Procedure Problems Delay ISFSI Project Startup; September 29, 2010

- IR 1121882; FHB Overhead Crane Operating Temperature Outside Procedure;

October 4, 2010

- IR 1121913; Procedure Changes Needed; October 4, 2010

- IR 1122498; NRC Questioned Items Apparently Stored Near ISFSI Pad; October 5, 2010

- IR 1122947; NRC Walkdown of ISFSI Storage Pad Area

- IR 1123339; FHB Crane Girder Temperature not met Before Use; October 7, 2010

- IR 1123564; ISFSI Mating Device Bolt Stuck

- IR 1124377; Need Temperature Instrument to meet FSAR Requirement; October 9, 2010

- IR 1125950; ISFSI Procedure Revision for BFP FH-71; October 13, 2010

- IR 1126491; ISFSI Bolts Need Evaluation to Establish Criteria; October, 12, 2010

- IR 1127060; ISFSI Annulus Cooling; October 15, 2010

- IR 1131564; ISFSI Annulus Temperature Analysis; October 27, 2010

- IR 1134848; NSRP Ops Subcommittee - ISFSI IPA Briefing; November 3, 2010

- IR 1135839; NOS Identified Issues with ISFSI Related Test Equipment; November 4, 2010

- IR 1138033; NRC Identified Rust Spots in Vents of HI-STORMS; November 9, 2010

- IR 1139597; Continuation of Root Cause Actions for IR 1107151; November 12, 2010

- IR 1139650; ISFSI Fuel Selection Gives Incorrect Max Assembly Enrichment,

November 12, 2010

- IR 1146205; Engineering Manager needs to Assign 72.212 Coordinator; November 30, 2010

- IR 1146276; Exelon Needs a Common 72.212 Report Change Process; November 30, 2010

- IR 1147090; NRC Identifies Procedure Enhancement; November 24, 2010

- 72.48-001; 72.212 Evaluation Report Change; Revision 0

- 72.48-002; 72.212 Evaluation Report Change 002; Revision 0

- 72.48-003; HI-TRAC Movement within the Fuel Building; Revision 0

- 72.48-004; Spent Fuel Cask Site Transportation; Revision 0

- 72.48-005; HI-TRAC Loading Operations; Revision 0

- 72.48-006; MPC Inspection; Revision 0

- 72.48-007; Transporter Operations; Revision 0

- 72.48-008; MPC Alternate Cooling; Revision 0

- 72.48-009; MPC Processing; Revision 0

- 72.48-010; Spent Fuel Cask Contingency Actions; Revision 0

- 72.48-011; MPC Processing; Revision 0

- 72.48-012; MPC Processing; Revision 0

- 72.48-013; HI-TRTAC Movement within the Fuel Building; Revision 0

- 72.48-014; HI-TRAC Loading Operations; Revision 0

- 72.48-015; MPC Alternate Cooling; Revision 0

- 72.48-016; Spent Fuel cask Contingency Actions; Revision 0

- 72.48-017; MPC Processing; Revision 0

- 72.48-018; HI-TRAC Movement within the Fuel Building; Revision 0

- 72.48-019; HI-TRAC Loading Operations; Revision 0

- 72.48-020; MPC Processing; Revision 0

- 72.48-021; MPC Alternate Cooling; Revision 0

- BFP FH-64; Transporter Operations; Revision 4

- BFP FH-65; Spent Fuel Cask Site Transportation; Revision 6

- BFP FH-68; HI-TRAC Preparation; Revision 2

- BFP FH-69; HI-TRAC Movement within the Fuel Building; Revision 4

- BFP FH-70; HI-TRAC Loading Operations; Revision 1

- BFP FH-71; MPC Processing; Revision 5

- BFP FH-71; MPC Processing; Revision 6

9 Attachment

- BFP FH-71; MPC Processing; Revision 7

- BFP FH-71; MPC Processing; Revision 8

- BFP FH-71; MPC Processing; Revision 9

- BFP FH-71; MPC Processing; Revision 10

- BFP FH-71; MPC Processing; Revision 11

- BFP FH-72; HI-STORM Processing; Revision 0

- BFP FH-78; Vacuum Drying System Operation; Revision 2

- BFP Fh-80; Haul Path and ISFSI Dry Run Operations; Revision 0

- BFP FH-83; Spent Fuel Cask Contingency Actions; Revision 1

- BFP FH-84; HI-TRAC Operations within the Fuel Handling Building; Revision 0

- BFP-FH-20; Operation of Fuel Handling Building Crane; Revision 24

- LS-BY-105; 72.48 Review Process for Dry Cask Storage; Revision 1

- NF-AP-622; Fuel Selection and Documentation for Dry Cask Storage; Revision 22

- Byron Nuclear Power Station, Units 1 and 2; 10 CFR 72.212 Evaluation Report; Revision 0

- Holtec Document 1676066; Responses to Potential URIs on Vacuum Drying / Annulus Flush;

September 30, 2010

- Holtec Document 1676066 R1; Responses to Potential URIs on Vacuum Drying / Annulus

Flush; October 6, 2010

- Apparent Cause Report 1100370; ISFSI Seismic Restraint Bumper Detached from Support

Arm

- ISFSI Campaign Risk Matrix

- Root Cause Report 1107151; Annulus Chiller Unit Trip and Associated Organization and

Programmatic Issues

- 2008 ISFSI Audit Comparative Report; November 6, 2008

- ISFSI Cask Loading Recovery Action Plan; August 30, 2010

- Registration of Use of Cask to Store Spent Fuel ; October 6, 2010

- Expectation for ISFSI Pad Cleanliness; October 15, 2010

- Holtec Document 1678064; VCT Tower Offset; October 22, 2010

- Holtec Document 1678064; Vacuum Drying/Annulus Flush of 21.22 kW MPC; Revision 1

10 Attachment

LIST OF ACRONYMS USED

AC Alternating Current

ADAMS Agencywide Document Access Management System

ASME American Society of Mechanical Engineers

AF Auxiliary Feedwater

CAP Corrective Action Program

CFR Code of Federal Regulations

ºF Degree Fahrenheit

DC Direct Current

EDG Emergency Diesel Generator

FHB Fuel Handling Building

FSAR Final Safety Analysis Report

FWIV Feedwater Isolation Valve

GL Generic Letter

HI-STORM Storage Cask

HI-TRAC Transfer Cask

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Issue Report

ISFSI Independent Spent Fuel Storage Installation

ISG Interim Staff Guidance

JPM Job Performance Measure

LER Licensee Event Report

LORT Licensed Operator Requalification Training

MPC Multi-Purpose Canister

MSPI Mitigating Systems Performance Indicator

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission

ODCM Occupational Dose Calculation Manual

OWA Operator Workaround

PARS Publicly Available Records System

PI Performance Indicator

RCS Reactor Coolant System

RETS Radiological Effluence Technical Specification

RSH River Screen House

SAT Systematic Approach to Training

S/G Steam Generator

SI Safety Injection

SPST Spent Fuel Storage and Transportation

SX Essential Service Water

SXCT Essential Service Water Cooling Tower

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

USAR Updated Safety Analysis Report

UHS Ultimate Heat Sink

11 Attachment

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eric R. Duncan, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454; 50-455;72-068

License Nos. NPF-37; NPF-66

Enclosure: Inspection Report 05000454/2010005; 05000455/2010005; 07200068/2010003

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

DOCUMENT NAME: G:\DRPIII\BYRO\Byron 2010 005.docx

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII

NAME RNg:dtp EDuncan

DATE 1/31/11 1/31/11

OFFICIAL RECORD COPY

Letter to M. Pacilio from E. Duncan dated January 31, 2011.

SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION

REPORT 05000454/2010-005; 05000455/2010-005; 07200068/2010003-2

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