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{{#Wiki_filter:ACCELERATEDDITRIBUTIONDEMONSTTIONSYSTEMREGULATORYINFORMATIONDXSRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9008270136DOC.DATE:90/08/17NOTARIZED:NODOCKETFACIL:50-315DonaldC.CookNuclearPowerPlant,Unit1,Indiana&0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,Indiana&05000316AUTH.NAMEAUTHORAFFILIATIONALEXICH,M.P.IndianaMichiganPowerCo.(formerlyIndiana&MichiganEleRECIP.NAMERECIPIENTAFFILXATIONMURLEY,T.E.DocumentControlBranch(DocumentControlDesk).II
{{#Wiki_filter:ACCELERATED DITRIBUTION DEMONSTTIONSYSTEMREGULATORY INFORMATION DXSRIBUTIONSYSTEM(RIDS)ACCESSION NBR:9008270136 DOC.DATE:
90/08/17NOTARIZED:
NODOCKETFACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,Indiana&0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,Indiana&05000316AUTH.NAMEAUTHORAFFILIATION ALEXICH,M.P.
IndianaMichiganPowerCo.(formerly Indiana&MichiganEleRECIP.NAME RECIPIENT AFFILXATION MURLEY,T.E.
DocumentControlBranch(Document ControlDesk).II


==SUBJECT:==
==SUBJECT:==
SubmitsinfotocloseoutcorrectiveactionsforSPDS,inresponsetoNRC900720ltr.DISTRIBUTIONCODE:A003DCOPIESRECEIVED:LTRlENCL6SIZE:3TITLE:OR/LicensingSubmittal:Suppl1toNUREG-0737(GenericLtr82-33)NOTES:RECIPIENTIDCODE/NAMEPD3-1LACOLBURN,T.INTERNAL:NRRJDLPQ/LHFB11R,01EXTERNAL:LPDRNSICCOPXESLTTRENCLRECIPIENTIDCODE/NAMEPD3-1PDOCgjLFMBRES/DSIR/EIBNRPDRCOPIESLTTRENCLNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.20079)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEED!jTOTALNUMBEROFCOPIESREQUIRED:LTTR11ENCL 0gClljrC IndianaMichiganPowerCompanyP.O.Box16631Columbus,OH43216IAEP:NRC:0773AIDonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74COOKNUCLEARPLANTSAFETYPARAMETERDISPLAYSYSTEM(SPDS)CORRECTIVEACTIONCLOSEOUTU.S.NuclearRegulatoryCommissionAttn:DocumentControlDeskWashington,D.C.20555Attn:T.E.MurleyAugust17,1990
Submitsinfotocloseoutcorrective actionsforSPDS,inresponsetoNRC900720ltr.DISTRIBUTION CODE:A003DCOPIESRECEIVED:LTR lENCL6SIZE:3TITLE:OR/Licensing Submittal:
Suppl1toNUREG-0737(Generic Ltr82-33)NOTES:RECIPIENT IDCODE/NAME PD3-1LACOLBURN,T.
INTERNAL:
NRRJDLPQ/LHFB11 R,01EXTERNAL:
LPDRNSICCOPXESLTTRENCLRECIPIENT IDCODE/NAME PD3-1PDOCgjLFMBRES/DSIR/EIBNRPDRCOPIESLTTRENCLNOTETOALL"RIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!jTOTALNUMBEROFCOPIESREQUIRED:
LTTR11ENCL 0gClljrC IndianaMichiganPowerCompanyP.O.Box16631Columbus, OH43216IAEP:NRC:0773AI DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74COOKNUCLEARPLANTSAFETYPARAMETER DISPLAYSYSTEM(SPDS)CORRECTIVE ACTIONCLOSEOUTU.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Attn:T.E.MurleyAugust17,1990


==DearDr.Murley:==
==DearDr.Murley:==
ThisletterrespondstoyourJuly20,1990,letterandprovidesconfirmationthatcorrectiveactioninresponsetothefindingsresultingfromtheon-siteauditoftheSPDShasbeentakenandtheitemsareclosed.Thespecificfindingsandourconfirmationofclose-outaregivenbelow.SPDSIsNotContinuousoTheSPDSmonitordoesnotprovideanyvisualoraudiblecuestoalertoperatorstoachangeinstatusforthefiveplant-specificsafetyfunctionsondisplaysotherthanthetwo,topleveliconicdisplays.R~esenseThemodificationtolimitthekeyboardfunctionsavailableononeofthecontrolroomTSCcomputerterminalsandprovideadedicateddisplayoftheSPDSiconicwascompletedonJuly2,1990,forbothUnits1and2.ThesoftwaremodificationpreventsauserfromaccessinganydisplaysotherthantheiconicdisplaysfromtheSPDS-dedicatedterminal.AlongrangesolutionisalsobeinginvestigatedthatwouldpermitausertoaccessotherdisplaysontheSPDSdedicatedterminalwhilestillbeingawareifanyadversechangestotheICONICDisplays'rocessvariables.Ifthisalternativesolutionisfoundtobepracticalitwillbeimplemented.SPDSIsNotDesinedtoIncororateAccetedHumanFactorsPrincilesoNumericalvaluesforthehighandlowlevelalarmsetpoints0"OG~9008270iM900Si7PDRADOCK05000315PPDCOo90y
ThisletterrespondstoyourJuly20,1990,letterandprovidesconfirmation thatcorrective actioninresponsetothefindingsresulting fromtheon-siteauditoftheSPDShasbeentakenandtheitemsareclosed.Thespecificfindingsandourconfirmation ofclose-out aregivenbelow.SPDSIsNotContinuous oTheSPDSmonitordoesnotprovideanyvisualoraudiblecuestoalertoperators toachangeinstatusforthefiveplant-specificsafetyfunctions ondisplaysotherthanthetwo,topleveliconicdisplays.
R~esenseThemodification tolimitthekeyboardfunctions available ononeofthecontrolroomTSCcomputerterminals andprovideadedicated displayoftheSPDSiconicwascompleted onJuly2,1990,forbothUnits1and2.Thesoftwaremodification preventsauserfromaccessing anydisplaysotherthantheiconicdisplaysfromtheSPDS-dedicated terminal.
Alongrangesolutionisalsobeinginvestigated thatwouldpermitausertoaccessotherdisplaysontheSPDSdedicated terminalwhilestillbeingawareifanyadversechangestotheICONICDisplays'rocess variables.
Ifthisalternative solutionisfoundtobepractical itwillbeimplemented.
SPDSIsNotDesinedtoIncororateAccetedHumanFactorsPrincilesoNumerical valuesforthehighandlowlevelalarmsetpoints 0"OG~9008270iM 900Si7PDRADOCK05000315PPDCOo90y


h\sDr.T.E.Murley-2-AEP:NRC:0773AIoneachsafetyfunction"spoke"ofthenarrow-andwide-rangeiconicdisplayswerenotidentified.Somealarmsetpointswerereactortripvaluesandotherswereeitheranticipatoryvaluesorsystemcapacityvalues.Inaddition,theUnit2SPDSsteamgeneratorlowlevelreactortripsetpoint,21%,wasincorrectlysetattheUnit1valueof17%.Inanothercase,theUnit1SPDShighTavgalarmsetpointontheSPDShadnotbeenchangedtoreflecttheamendedTechnicalSpecificationvalue.R~esonseTheapparentdisparityintheselectionofreactortrip'alues,systemcapacityvalues,oranticipatoryvalueshasbeenrectified.Thenarrow-rangesteamgeneratorlevellowlimitontheUnit2narrow-rangeiconicdisplaywaschangedtothecorrectreactortripsetpoint.TheRCSaveragetemperaturehighlimitontheUnit1narrow-rangeiconicdisplayhasbeenchangedtothecorrectvaluecorrespondingtotheamendedTechnicalSpecificationlimitingconditionforoperationrequirement.0eratorTraininWithSPDSWasNotSatisfactoroControlroomdidnotknow,inallinstances,whatthenumericalvalueswereforthehighandlowlevelalarmsetpointsforeachsafetyfunctionontheSPDSnarrow-andwide-rangeiconicdisplays.~ResonseNumericalvaluesforthealarmlimitsontheiconicdisplayhavebeenincorporatedintothePlantOperatorstechnicaldatareference.Thegeneralphilosophyonhowthesevalueswereselectedwasincorporatedintotheoperatorrequalificationtrainingbeginninginthethirdquarterof1990.ThisdocumenthasbeenpreparedfollowingCorporateproceduresthatincorporateareasonablesetofcontrolstoensureitsaccuracyandcompletenesspriortosignaturebytheundersigned.Sincerely,M.P.AlechVicePresident Ag~~~'Dr.T.E.Murley-3-AEP:NRC:0773AIehcc:D.H.Williams,Jr.A.A.Blind-BridgmanJ.R.PadgettG.CharnoffNFEMSectionChiefA.B.Davis-RegionIIINRCResidentInspector-Bridgman ff.e'7~~4}}
h\sDr.T.E.Murley-2-AEP:NRC:0773AI oneachsafetyfunction"spoke"ofthenarrow-andwide-range iconicdisplayswerenotidentified.
Somealarmsetpoints werereactortripvaluesandotherswereeitheranticipatory valuesorsystemcapacityvalues.Inaddition, theUnit2SPDSsteamgenerator lowlevelreactortripsetpoint, 21%,wasincorrectly setattheUnit1valueof17%.Inanothercase,theUnit1SPDShighTavgalarmsetpointontheSPDShadnotbeenchangedtoreflecttheamendedTechnical Specification value.R~esonseTheapparentdisparity intheselection ofreactortrip'alues,systemcapacityvalues,oranticipatory valueshasbeenrectified.
Thenarrow-range steamgenerator levellowlimitontheUnit2narrow-range iconicdisplaywaschangedtothecorrectreactortripsetpoint.
TheRCSaveragetemperature highlimitontheUnit1narrow-range iconicdisplayhasbeenchangedtothecorrectvaluecorresponding totheamendedTechnical Specification limitingcondition foroperation requirement.
0eratorTraininWithSPDSWasNotSatisfactor oControlroomdidnotknow,inallinstances, whatthenumerical valueswereforthehighandlowlevelalarmsetpoints foreachsafetyfunctionontheSPDSnarrow-andwide-range iconicdisplays.
~ResonseNumerical valuesforthealarmlimitsontheiconicdisplayhavebeenincorporated intothePlantOperators technical datareference.
Thegeneralphilosophy onhowthesevalueswereselectedwasincorporated intotheoperatorrequalification trainingbeginning inthethirdquarterof1990.Thisdocumenthasbeenpreparedfollowing Corporate procedures thatincorporate areasonable setofcontrolstoensureitsaccuracyandcompleteness priortosignature bytheundersigned.
Sincerely, M.P.AlechVicePresident Ag~~~'Dr.T.E.Murley-3-AEP:NRC:0773AI ehcc:D.H.Williams, Jr.A.A.Blind-BridgmanJ.R.PadgettG.CharnoffNFEMSectionChiefA.B.Davis-RegionIIINRCResidentInspector
-Bridgman ff.e'7~~4}}

Revision as of 07:51, 29 June 2018

Responds to NRC 900720 Ltr Re Violations Noted in Onsite Audit of Spds.Corrective Actions:Apparent Disparity in Selection of Reactor Trip & Sys Capacity or Anticipatory Values Rectified
ML17328A390
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/17/1990
From: ALEXICH M P
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: MURLEY T E
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:0773AI, AEP:NRC:773AI, NUDOCS 9008270136
Download: ML17328A390 (7)


Text

ACCELERATED DITRIBUTION DEMONSTTIONSYSTEMREGULATORY INFORMATION DXSRIBUTIONSYSTEM(RIDS)ACCESSION NBR:9008270136 DOC.DATE:

90/08/17NOTARIZED:

NODOCKETFACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,Indiana&0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,Indiana&05000316AUTH.NAMEAUTHORAFFILIATION ALEXICH,M.P.

IndianaMichiganPowerCo.(formerly Indiana&MichiganEleRECIP.NAME RECIPIENT AFFILXATION MURLEY,T.E.

DocumentControlBranch(Document ControlDesk).II

SUBJECT:

Submitsinfotocloseoutcorrective actionsforSPDS,inresponsetoNRC900720ltr.DISTRIBUTION CODE:A003DCOPIESRECEIVED:LTR lENCL6SIZE:3TITLE:OR/Licensing Submittal:

Suppl1toNUREG-0737(Generic Ltr82-33)NOTES:RECIPIENT IDCODE/NAME PD3-1LACOLBURN,T.

INTERNAL:

NRRJDLPQ/LHFB11 R,01EXTERNAL:

LPDRNSICCOPXESLTTRENCLRECIPIENT IDCODE/NAME PD3-1PDOCgjLFMBRES/DSIR/EIBNRPDRCOPIESLTTRENCLNOTETOALL"RIDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!jTOTALNUMBEROFCOPIESREQUIRED:

LTTR11ENCL 0gClljrC IndianaMichiganPowerCompanyP.O.Box16631Columbus, OH43216IAEP:NRC:0773AI DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74COOKNUCLEARPLANTSAFETYPARAMETER DISPLAYSYSTEM(SPDS)CORRECTIVE ACTIONCLOSEOUTU.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Attn:T.E.MurleyAugust17,1990

DearDr.Murley:

ThisletterrespondstoyourJuly20,1990,letterandprovidesconfirmation thatcorrective actioninresponsetothefindingsresulting fromtheon-siteauditoftheSPDShasbeentakenandtheitemsareclosed.Thespecificfindingsandourconfirmation ofclose-out aregivenbelow.SPDSIsNotContinuous oTheSPDSmonitordoesnotprovideanyvisualoraudiblecuestoalertoperators toachangeinstatusforthefiveplant-specificsafetyfunctions ondisplaysotherthanthetwo,topleveliconicdisplays.

R~esenseThemodification tolimitthekeyboardfunctions available ononeofthecontrolroomTSCcomputerterminals andprovideadedicated displayoftheSPDSiconicwascompleted onJuly2,1990,forbothUnits1and2.Thesoftwaremodification preventsauserfromaccessing anydisplaysotherthantheiconicdisplaysfromtheSPDS-dedicated terminal.

Alongrangesolutionisalsobeinginvestigated thatwouldpermitausertoaccessotherdisplaysontheSPDSdedicated terminalwhilestillbeingawareifanyadversechangestotheICONICDisplays'rocess variables.

Ifthisalternative solutionisfoundtobepractical itwillbeimplemented.

SPDSIsNotDesinedtoIncororateAccetedHumanFactorsPrincilesoNumerical valuesforthehighandlowlevelalarmsetpoints 0"OG~9008270iM 900Si7PDRADOCK05000315PPDCOo90y

h\sDr.T.E.Murley-2-AEP:NRC:0773AI oneachsafetyfunction"spoke"ofthenarrow-andwide-range iconicdisplayswerenotidentified.

Somealarmsetpoints werereactortripvaluesandotherswereeitheranticipatory valuesorsystemcapacityvalues.Inaddition, theUnit2SPDSsteamgenerator lowlevelreactortripsetpoint, 21%,wasincorrectly setattheUnit1valueof17%.Inanothercase,theUnit1SPDShighTavgalarmsetpointontheSPDShadnotbeenchangedtoreflecttheamendedTechnical Specification value.R~esonseTheapparentdisparity intheselection ofreactortrip'alues,systemcapacityvalues,oranticipatory valueshasbeenrectified.

Thenarrow-range steamgenerator levellowlimitontheUnit2narrow-range iconicdisplaywaschangedtothecorrectreactortripsetpoint.

TheRCSaveragetemperature highlimitontheUnit1narrow-range iconicdisplayhasbeenchangedtothecorrectvaluecorresponding totheamendedTechnical Specification limitingcondition foroperation requirement.

0eratorTraininWithSPDSWasNotSatisfactor oControlroomdidnotknow,inallinstances, whatthenumerical valueswereforthehighandlowlevelalarmsetpoints foreachsafetyfunctionontheSPDSnarrow-andwide-range iconicdisplays.

~ResonseNumerical valuesforthealarmlimitsontheiconicdisplayhavebeenincorporated intothePlantOperators technical datareference.

Thegeneralphilosophy onhowthesevalueswereselectedwasincorporated intotheoperatorrequalification trainingbeginning inthethirdquarterof1990.Thisdocumenthasbeenpreparedfollowing Corporate procedures thatincorporate areasonable setofcontrolstoensureitsaccuracyandcompleteness priortosignature bytheundersigned.

Sincerely, M.P.AlechVicePresident Ag~~~'Dr.T.E.Murley-3-AEP:NRC:0773AI ehcc:D.H.Williams, Jr.A.A.Blind-BridgmanJ.R.PadgettG.CharnoffNFEMSectionChiefA.B.Davis-RegionIIINRCResidentInspector

-Bridgman ff.e'7~~4