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| issue date = 11/12/1991
| issue date = 11/12/1991
| title = Lists Results of Secondary Containment Leak Rate Test Performed on Reactor Bldg.Test Demonstrated That Unit 3 Matl Interlock Outer Door Has Adequate Sealing to Maintain Secondary Containment Integrity
| title = Lists Results of Secondary Containment Leak Rate Test Performed on Reactor Bldg.Test Demonstrated That Unit 3 Matl Interlock Outer Door Has Adequate Sealing to Maintain Secondary Containment Integrity
| author name = EENIGENBURG E
| author name = Eenigenburg E
| author affiliation = COMMONWEALTH EDISON CO.
| author affiliation = COMMONWEALTH EDISON CO.
| addressee name = DAVIS A B
| addressee name = Davis A
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
| docket = 05000237, 05000249
| docket = 05000237, 05000249
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:ACCELERATED DISTIUBUTION DEMONST$QTIONSYSTEMREGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)'ACCESSION NBR:9112260334 DOC.DATE:
{{#Wiki_filter:ACCELERATED DISTIUBUTION DEMONST$Q TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
91/11/12NOTARIZED:
'ACCESSION NBR:9112260334                   DOC.DATE:   91/11/12  NOTARIZED: NO          DOCKET FACIL:50-237 Dresden Nuclear Power Station, Unit 2, Commonwealth                     E 05000237 50-249 Dresden Nuclear Power Station, Unit 3, Commonwealth                   E 05000249 AUTH. NAME             , AUTHOR AFFILIATION EENIGENBURG,E.             Commonwealth Edison Co.
NOFACIL:50-237 DresdenNuclearPowerStation,Unit2,Commonwealth E50-249DresdenNuclearPowerStation,Unit3,Commonwealth EAUTH.NAME,AUTHORAFFILIATION EENIGENBURG,E.
RECIP.NAME                 RECIPIENT AFFILIATION DAVIS,A.B.         =
Commonwealth EdisonCo.RECIP.NAME RECIPIENT AFFILIATION DAVIS,A.B.
Region 3 (Post 820201)
=Region3(Post820201)


==SUBJECT:==
==SUBJECT:==
Listsresultsofsecondary containment leakratetestperformed onreactorbldg.Testdemonstrated thatUnit3matlinterlock outerdoorhasadequatesealingtomaintainsecondary containment-integrity.
Lists results of secondary containment leak rate test performed on reactor bldg. Test demonstrated that Unit 3 matl interlock outer door has adequate sealing to maintain secondary containment-integrity.
DISTRIBUTION CODE:IEOIDCOPIESRECEIVED:LTR (ENCL8SIZE:TITLE:General(50Dkt)-Insp Rept/Notice ofViolation ResponseDOCKET0500023705000249NOTES:License Expdateinaccordance with10CFR2,2.109(12/22/72).
DISTRIBUTION CODE: IEOID                COPIES RECEIVED:LTR     ( ENCL    8  SIZE:
05000237RECIPIENT 1DCODE/NAME PD3-2PDINTERNAL:
TITLE: General           (50  Dkt)-Insp Rept/Notice of Violation Response NOTES:License Exp            date in accordance with 10CFR2,2.109(12/22/72).           05000237 RECIPIENT              COPIES            RECIPIENT          COPIES 1D  CODE/NAME          LTTR E CL        ID CODE/NAME       LTTR ENCL PD3-2 PD                        1            SIEGEL,B.
ACRSAEOD/DEIIB DEDRONRRMORISSEAU,D I'I!'?ii/DLPQ/LPEB10 NRR/DREP/PEPB9H NPR/PMAS/ILRB12 PGFI02EXTERNAL:
INTERNAL: ACRS                                            AEOD AEOD/DEIIB                                   AEOD/DSP/TPAB DEDRO                                        NRR HARBUCK~ C ~
EGFrG/BRYCE,J.
NRR MORISSEAU,D                               NRR/DLPQ/LHFBPT I'I!'? ii/DLPQ/LPEB10                         NRR/DOEA/OEAB NRR/DREP/PEPB9H                               NRR/DST/DIR SE2 NPR/PMAS/ILRB12                               NUDOCS-ABSTRACT OGC/HDS2 PG    FI          02                      RGN3    FILE  01 EXTERNAL: EGFrG/BRYCE,J. H.                               NRC PDR N&IC NOTE TO ALL "RIDS" RECIPIENTS:
H.N&ICCOPIESLTTRECL1RECIPIENT IDCODE/NAME SIEGEL,B.
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
AEODAEOD/DSP/TPAB NRRHARBUCK~C~NRR/DLPQ/LHFBPT NRR/DOEA/OEAB NRR/DST/DIR SE2NUDOCS-ABSTRACT OGC/HDS2RGN3FILE01NRCPDRCOPIESLTTRENCLNOTETOALL"RIDS"RECIPIENTS:
TOTAL NUI!!'.".R OF COPIES REQUIRED: LTTR                24  ENCL
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!TOTALNUI!!'.".R OFCOPIESREQUIRED:
LTTR24ENCL


Commo~alth EdisonDresdenN~rPowerStationR.R.g1Morris,Illinois60450Telephone 815/942-2920 November12,1991EDELTR:091-700PRIPltIyy P0>eMr.A.BertDavisRegionalAdministrator Directorate ofRegulatory Operations RegionIIIU.S.NuclearRegulatory Commission 799Roosevelt RoadGlenEllyn,Illinois60137FJlf~+
Commo~alth             Edison Dresden      N~r Power Station R.R. g1 Morris, Illinois 60450 Telephone 815/942-2920 November 12, 1991 PRIPltIyy P0>
e EDE LTR:   091-700 Mr. A. Bert Davis Regional Administrator Directorate of Regulatory Operations Region  III F Jl f~+
U.S. Nuclear Regulatory Commission 799  Roosevelt Road Glen  Ellyn, Illinois        60137


==Subject:==
==Subject:==
Secondary Containment LeakRateTestingDresdenNuclearPowerStationCommonwealth EdisonCompanyDocketNos.50-237and50-249DearMr.DavisAspartoftheDresdenUnit3pre-outage workaSecondary Containment LeakRateTest(SCLRT)wasperformed ontheUnit2/3ReactorBuilding.
Secondary Containment Leak Rate Testing Dresden Nuclear Power Station Commonwealth Edison Company Docket Nos. 50-237 and 50-249 Dear Mr. Davis As  part of the Dresden Unit 3 pre-outage work a Secondary Containment Leak Rate Test (SCLRT) was performed on the Unit 2/3 Reactor Building.
TheSCLRTwasperformed inaccordance withDresdenUnit3Technical Specification 4.7.C.l.a.,
The SCLRT was performed in accordance with Dresden Unit 3 Technical Specification 4.7.C.l.a., which requires that prior to refueling, Secondary Containment integrity must be demonstrated by maintaining )/=
whichrequiresthatpriortorefueling, Secondary Containment integrity mustbedemonstrated bymaintaining
0.25 inches of water vacuum in the Reactor Building with one train of the Standby Gas Treatment system operating at a flow of </= 4000 cubic feet per minute (CFM) under calm wind conditions (</= 5 miles per hour). On September 07, 1991, the SCLRT was performed in accordance with Dresden Technical Staff Surveillance (DTS) Procedure 1600-22. The results of the test are listed    below.'2 U3 RX BLDG        U3 RX BLDG            SCLRT RX BLDG                U2 RX BLDG        MAT'L INTER-       MAT'L INTER-           RESULT, TRACKWAY INNER              TRACKWAY OUTER    LOCK INNER        LOCK OUTER            INCHES OF QQQKLQMXXQH            MhXEMK    .
)/=0.25inchesofwatervacuumintheReactorBuildingwithonetrainoftheStandbyGasTreatment systemoperating ataflowof</=4000cubicfeetperminute(CFM)undercalmwindconditions
CLOSED                    CLOSED            CLOSED            CLOSED                -0.273 CLOSED                    CLOSED          OPEN              CLOSED                -0.191 OPEN                      CLOSED            CLOSED            CLOSED                -0.268 ZEDE91/447
(</=5milesperhour).OnSeptember 07,1991,theSCLRTwasperformed inaccordance withDresdenTechnical StaffSurveillance (DTS)Procedure 1600-22.Theresultsofthetestarelistedbelow.'2RXBLDGTRACKWAYINNERU2RXBLDGTRACKWAYOUTERU3RXBLDGMAT'LINTER-LOCKINNERU3RXBLDGMAT'LINTER-LOCKOUTERQQQKLQMXXQH SCLRTRESULT,INCHESOFMhXEMK.CLOSEDCLOSEDOPENCLOSEDCLOSEDCLOSEDCLOSEDOPENCLOSEDCLOSEDCLOSEDCLOSED-0.273-0.191-0.268ZEDE91/447
                                                                                          /For
/For  
 
'
As shown in the above table, the result with  all  interlock doors closed was 0.273 inches of water negative pressure in secondary containment with respect to atmosphere, which satisfied the Technical Specification 4.7.C.l.a. requirement. This SCLRT also demonstrated that the Unit 2 Reactor Building trackway interlock outer door has adequate sealing to maintain secondary containment integrity. Additionally, this test demonstrated that the Unit 3 material interlock outer door does not have adequate sealing to maintain secondary containment integrity. Dresden Administrative Procedure (DAP) 13-14, Unit 3 Reactor Building Material Interlock Access Control, is a posted procedure and provides adequate control of this interlock.
Asshownintheabovetable,theresultwithallinterlock doorsclosedwas0.273inchesofwaternegativepressureinsecondary containment withrespecttoatmosphere, whichsatisfied theTechnical Specification 4.7.C.l.a.
This report is being submitted in accordance with Section 6.6.C.3.h. of the Unit 2 and Unit 3 Technical Specifications. Please direct any requests for further information regarding this topic to M. Blakemore, Technical Staff Systems Engineer, at extension 2421.
requirement.
Sincerely E. D. Eenigenburg Station Manager Dresden Nuclear Power  Station cc~ M. Strait S. Lawson G. Smith J. Kotowski L. Gerner M. Blakemore File/NRC File/Numerical ZEDE91/447}}
ThisSCLRTalsodemonstrated thattheUnit2ReactorBuildingtrackwayinterlock outerdoorhasadequatesealingtomaintainsecondary containment integrity.
Additionally, thistestdemonstrated thattheUnit3materialinterlock outerdoordoesnothaveadequatesealingtomaintainsecondary containment integrity.
DresdenAdministrative Procedure (DAP)13-14,Unit3ReactorBuildingMaterialInterlock AccessControl,isapostedprocedure andprovidesadequatecontrolofthisinterlock.
Thisreportisbeingsubmitted inaccordance withSection6.6.C.3.h.
oftheUnit2andUnit3Technical Specifications.
Pleasedirectanyrequestsforfurtherinformation regarding thistopictoM.Blakemore, Technical StaffSystemsEngineer, atextension 2421.Sincerely E.D.Eenigenburg StationManagerDresdenNuclearPowerStationcc~M.StraitS.LawsonG.SmithJ.KotowskiL.GernerM.Blakemore File/NRCFile/Numerical ZEDE91/447}}

Latest revision as of 16:29, 3 February 2020

Lists Results of Secondary Containment Leak Rate Test Performed on Reactor Bldg.Test Demonstrated That Unit 3 Matl Interlock Outer Door Has Adequate Sealing to Maintain Secondary Containment Integrity
ML18037A079
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 11/12/1991
From: Eenigenburg E
COMMONWEALTH EDISON CO.
To: Davis A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
EDE-LTR-91-700, NUDOCS 9112260334
Download: ML18037A079 (6)


Text

ACCELERATED DISTIUBUTION DEMONST$Q TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

'ACCESSION NBR:9112260334 DOC.DATE: 91/11/12 NOTARIZED: NO DOCKET FACIL:50-237 Dresden Nuclear Power Station, Unit 2, Commonwealth E 05000237 50-249 Dresden Nuclear Power Station, Unit 3, Commonwealth E 05000249 AUTH. NAME , AUTHOR AFFILIATION EENIGENBURG,E. Commonwealth Edison Co.

RECIP.NAME RECIPIENT AFFILIATION DAVIS,A.B. =

Region 3 (Post 820201)

SUBJECT:

Lists results of secondary containment leak rate test performed on reactor bldg. Test demonstrated that Unit 3 matl interlock outer door has adequate sealing to maintain secondary containment-integrity.

DISTRIBUTION CODE: IEOID COPIES RECEIVED:LTR ( ENCL 8 SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:License Exp date in accordance with 10CFR2,2.109(12/22/72). 05000237 RECIPIENT COPIES RECIPIENT COPIES 1D CODE/NAME LTTR E CL ID CODE/NAME LTTR ENCL PD3-2 PD 1 SIEGEL,B.

INTERNAL: ACRS AEOD AEOD/DEIIB AEOD/DSP/TPAB DEDRO NRR HARBUCK~ C ~

NRR MORISSEAU,D NRR/DLPQ/LHFBPT I'I!'? ii/DLPQ/LPEB10 NRR/DOEA/OEAB NRR/DREP/PEPB9H NRR/DST/DIR SE2 NPR/PMAS/ILRB12 NUDOCS-ABSTRACT OGC/HDS2 PG FI 02 RGN3 FILE 01 EXTERNAL: EGFrG/BRYCE,J. H. NRC PDR N&IC NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUI!!'.".R OF COPIES REQUIRED: LTTR 24 ENCL

Commo~alth Edison Dresden N~r Power Station R.R. g1 Morris, Illinois 60450 Telephone 815/942-2920 November 12, 1991 PRIPltIyy P0>

e EDE LTR: 091-700 Mr. A. Bert Davis Regional Administrator Directorate of Regulatory Operations Region III F Jl f~+

U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137

Subject:

Secondary Containment Leak Rate Testing Dresden Nuclear Power Station Commonwealth Edison Company Docket Nos. 50-237 and 50-249 Dear Mr. Davis As part of the Dresden Unit 3 pre-outage work a Secondary Containment Leak Rate Test (SCLRT) was performed on the Unit 2/3 Reactor Building.

The SCLRT was performed in accordance with Dresden Unit 3 Technical Specification 4.7.C.l.a., which requires that prior to refueling, Secondary Containment integrity must be demonstrated by maintaining )/=

0.25 inches of water vacuum in the Reactor Building with one train of the Standby Gas Treatment system operating at a flow of </= 4000 cubic feet per minute (CFM) under calm wind conditions (</= 5 miles per hour). On September 07, 1991, the SCLRT was performed in accordance with Dresden Technical Staff Surveillance (DTS) Procedure 1600-22. The results of the test are listed below.'2 U3 RX BLDG U3 RX BLDG SCLRT RX BLDG U2 RX BLDG MAT'L INTER- MAT'L INTER- RESULT, TRACKWAY INNER TRACKWAY OUTER LOCK INNER LOCK OUTER INCHES OF QQQKLQMXXQH MhXEMK .

CLOSED CLOSED CLOSED CLOSED -0.273 CLOSED CLOSED OPEN CLOSED -0.191 OPEN CLOSED CLOSED CLOSED -0.268 ZEDE91/447

/For

As shown in the above table, the result with all interlock doors closed was 0.273 inches of water negative pressure in secondary containment with respect to atmosphere, which satisfied the Technical Specification 4.7.C.l.a. requirement. This SCLRT also demonstrated that the Unit 2 Reactor Building trackway interlock outer door has adequate sealing to maintain secondary containment integrity. Additionally, this test demonstrated that the Unit 3 material interlock outer door does not have adequate sealing to maintain secondary containment integrity. Dresden Administrative Procedure (DAP) 13-14, Unit 3 Reactor Building Material Interlock Access Control, is a posted procedure and provides adequate control of this interlock.

This report is being submitted in accordance with Section 6.6.C.3.h. of the Unit 2 and Unit 3 Technical Specifications. Please direct any requests for further information regarding this topic to M. Blakemore, Technical Staff Systems Engineer, at extension 2421.

Sincerely E. D. Eenigenburg Station Manager Dresden Nuclear Power Station cc~ M. Strait S. Lawson G. Smith J. Kotowski L. Gerner M. Blakemore File/NRC File/Numerical ZEDE91/447