IR 05000255/2017003: Difference between revisions

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| number = ML17299A146
| number = ML17299A146
| issue date = 10/25/2017
| issue date = 10/25/2017
| title = Palisades Nuclear Plant - NRC Integrated Inspection Report 05000255/2017003
| title = NRC Integrated Inspection Report 05000255/2017003
| author name = Duncan E
| author name = Duncan E
| author affiliation = NRC/RGN-III/DRP/B3
| author affiliation = NRC/RGN-III/DRP/B3
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=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUITE 210 LISLE, ILLINOIS 60532-4352 October 25, 2017 Mr. Charles Arnone Vice President, Operations Entergy Nuclear Operations, Inc. Palisades Nuclear Plant 27780 Blue Star Memorial Highway Covert, MI 49043-9530
{{#Wiki_filter:UNITED STATES October 25, 2017


SUBJECT: PALISADES NUCLEAR PLANT-NRC INTEGRATED INSPECTION REPORT 05000255/2017003
==SUBJECT:==
PALISADES NUCLEAR PLANTNRC INTEGRATED INSPECTION REPORT 05000255/2017003


==Dear Mr. Arnone:==
==Dear Mr. Arnone:==
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Palisades Nuclear Plant. On October 18, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The enclosed report represents the results of this inspection.
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Palisades Nuclear Plant. On October 18, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The enclosed report represents the results of this inspection.


Based on the results of this inspection, the NRC has identified one issue that was evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has also determined that a violation is associated with this issue. Because condition reports were initiated to address this issue, this violation is being treated as a  
Based on the results of this inspection, the NRC has identified one issue that was evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has also determined that a violation is associated with this issue. Because condition reports were initiated to address this issue, this violation is being treated as a Non-Cited Violation (NCV), consistent with Section 2.3.2 of the NRC Enforcement Policy. This NCV is described in the subject inspection report. Further, the inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.


Non-Cited Violation (NCV), consistent with Section 2.3.2 of the NRC Enforcement Policy. This NCV is described in the subject inspection report. Further, the inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a NCV consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest the violation or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Palisades Nuclear Plant. In addition, if you disagree with the cross-cutting aspect assignment to the finding discussed in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Palisades Nuclear Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
If you contest the violation or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Palisades Nuclear Plant.


Sincerely,/RA/ Eric Duncan, Chief Branch 3
In addition, if you disagree with the cross-cutting aspect assignment to the finding discussed in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Palisades Nuclear Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.


Division of Reactor Projects Docket No. 50-255 License No. DPR-20  
Sincerely,
 
/RA/
===Enclosure:===
Eric Duncan, Chief Branch 3 Division of Reactor Projects Docket No. 50-255 License No. DPR-20 Enclosure:
Inspection Report 05000255/2017003 cc: Distribution via LISTSERV
Inspection Report 05000255/2017003 cc: Distribution via LISTSERV


=SUMMARY=
=SUMMARY=
Inspection Report 05000255/2017003, 07/01/2017 - 09/30/2017; Palisades Nuclear Plant; Problem Identification & Resolution. This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. One Green finding was identified by the inspectors.
Inspection Report 05000255/2017003, 07/01/2017 - 09/30/2017; Palisades Nuclear Plant;
 
Problem Identification & Resolution.
 
This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. One Green finding was identified by the inspectors.


The finding involved a Non-Cited Violation (NCV) of U.S. Nuclear Regulatory Commission (NRC) requirements. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," dated April 29, 2015.
The finding involved a Non-Cited Violation (NCV) of U.S. Nuclear Regulatory Commission (NRC) requirements. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," dated April 29, 2015.


Cross-cutting aspects are determined using IMC 0310, "Aspects Within the Cross-Cutting Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6.
Cross-cutting aspects are determined using IMC 0310, "Aspects Within the Cross-Cutting Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision  


===NRC Identified===
===NRC Identified===
and Self-Revealed Findings  
and Self-Revealed Findings


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
A finding of very low safety significance and an associated NCV of Technical Specification (TS) 5.4.1, "Procedures," was self-revealed on March 31, 2017, when the 1-2 Diesel Generator (DG) tripped during performance of monthly TS surveillance procedure MO-7A-2, "Emergency Diesel Generator 1-2.Specifically, during conduct of the monthly surveillance procedure, restoration activities associated with maintenance of breaker 152-213, 1-2 DG to Bus 1D, were being performed. When maintenance personnel closed the trip cutouts for the Z-phase of the 1-2 DG differential overcurrent relay, an unbalanced current flow into the differential relay resulted in relay actuation. This actuation resulted in a trip of the output breaker and subsequently the 1-2 DG. The trip caused a delay in the TS surveillance activities and resulted in the extended unavailability and inoperability of the 1-2 DG. The licensee entered this issue into their corrective action program (CAP) as condition report (CR) CR-PLP-2017-01291.
A finding of very low safety significance and an associated NCV of Technical Specification (TS) 5.4.1, Procedures, was self-revealed on March 31, 2017, when the 1-2 Diesel Generator (DG) tripped during performance of monthly TS surveillance procedure MO-7A-2, Emergency Diesel Generator 1-2. Specifically, during conduct of the monthly surveillance procedure, restoration activities associated with maintenance of breaker 152-213, 1-2 DG to Bus 1D, were being performed. When maintenance personnel closed the trip cutouts for the Z-phase of the 1-2 DG differential overcurrent relay, an unbalanced current flow into the differential relay resulted in relay actuation.


Corrective actions included retesting the 1-2 DG and updating the work instructions associated with the differential overcurrent relays to include caution statements that opening or closing trip cutouts for the relays while the output breakers from the DGs to the associated buses were closed could cause the differential relays to actuate and trip the DG. The issue was determined to be more than minor in accordance with IMC 0612, Appendix B, "Issue Screening," because it was associated with the Mitigating Systems cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding screened as having very low safety significance (Green) in accordance with IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," Exhibit 2, since the inspectors answered "No" to all screening questions. The finding had a cross-cutting aspect in the area of Human Performance, in the Work Management aspect, for the licensee's failure to identify and manage risk commensurate to the work (H.5). (Section 4OA2)3
This actuation resulted in a trip of the output breaker and subsequently the 1-2 DG. The trip caused a delay in the TS surveillance activities and resulted in the extended unavailability and inoperability of the 1-2 DG. The licensee entered this issue into their corrective action program (CAP) as condition report (CR) CR-PLP-2017-01291.
 
Corrective actions included retesting the 1-2 DG and updating the work instructions associated with the differential overcurrent relays to include caution statements that opening or closing trip cutouts for the relays while the output breakers from the DGs to the associated buses were closed could cause the differential relays to actuate and trip the DG.
 
The issue was determined to be more than minor in accordance with IMC 0612,
Appendix B, Issue Screening, because it was associated with the Mitigating Systems cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding screened as having very low safety significance (Green) in accordance with IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, since the inspectors answered No to all screening questions. The finding had a cross-cutting aspect in the area of Human Performance, in the Work Management aspect, for the licensees failure to identify and manage risk commensurate to the work (H.5). (Section 4OA2)
 
===Licensee-Identified Violations===


=== Licensee-Identified Violations===
A violation of very low safety significance or Severity Level IV that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's CAP. This violation and corrective action tracking number is listed in Section 4OA7 of this report.
A violation of very low safety significance or Severity Level IV that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's CAP. This violation and corrective action tracking number is listed in Section 4OA7 of this report.


4
=REPORT DETAILS=
 
===Summary of Plant Status===


=REPORT DETAILS=
The plant began the inspection period operating at full power. The unit operated at or near full power for the entire inspection period.
Summary of Plant Status The plant began the inspection period operating at full power. The unit operated at or near full power for the entire inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
{{IP sample|IP=IP 71111.01}}
===.1 Readiness for Impending Adverse Weather Condition-Geo-Magnetic Storm Forecast===
===.1 Readiness for Impending Adverse Weather ConditionGeo-Magnetic Storm Forecast===


====a. Inspection Scope====
====a. Inspection Scope====
A geo-magnetic storm disturbance with a K-index greater than or equal to seven with the potential to influence the plant was forecast on September 7, 2017. The inspectors reviewed the licensee's preparations for the impending weather conditions and conducted independent walkdowns of the plant's alternating current (AC) power systems. The inspectors verified that plant procedures for the reliability and continued availability of the offsite and onsite power systems were appropriate. The inspectors also reviewed the licensee's communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged in a timely manner when issues arose to take any necessary actions. The inspectors reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment to this report. This inspection constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure (IP) 71111.01-05.
A geo-magnetic storm disturbance with a K-index greater than or equal to seven with the potential to influence the plant was forecast on September 7, 2017. The inspectors reviewed the licensees preparations for the impending weather conditions and conducted independent walkdowns of the plants alternating current (AC) power systems. The inspectors verified that plant procedures for the reliability and continued availability of the offsite and onsite power systems were appropriate. The inspectors also reviewed the licensees communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged in a timely manner when issues arose to take any necessary actions. The inspectors reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure (IP) 71111.01-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial system walkdowns of the following risk-significant systems:  
The inspectors performed partial system walkdowns of the following risk-significant systems:
* 'B' high pressure safety injection train;  
* B high pressure safety injection train;
* 'B' service water train; and
* B service water train; and
* alternate chemical and volume control system dilution pathway. The inspectors selected these systems based on their risk significance relative to the Reactor Safety cornerstones at the time they were inspected. The inspectors attempted 5 to identify any discrepancies that could impact the function of the system and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures,
* alternate chemical and volume control system dilution pathway.


system diagrams, the Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.
The inspectors selected these systems based on their risk significance relative to the Reactor Safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.


The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved
The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.


equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this  
The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.


report. These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.
These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns which were focused on the availability, accessibility, and condition of firefighting equipment in the following risk-significant plant areas:
The inspectors conducted fire protection walkdowns which were focused on the availability, accessibility, and condition of firefighting equipment in the following risk-significant plant areas:
* Fire Areas 6 & 8: diesel generator (DG) 1-2 and fuel oil day tank rooms, elevation 590';
* Fire Areas 6 & 8: diesel generator (DG) 1-2 and fuel oil day tank rooms, elevation 590;
* Fire Areas 5 & 7: DG 1-1 and fuel oil day tank rooms, elevation 590';
* Fire Areas 5 & 7: DG 1-1 and fuel oil day tank rooms, elevation 590;
* Fire Area 26: southwest cable penetration room, elevations 590' and 607';
* Fire Area 26: southwest cable penetration room, elevations 590 and 607;
* Fire Area 3: 1D switchgear room and north cableway, elevations 607' and 625';
* Fire Area 3: 1D switchgear room and north cableway, elevations 607 and 625';
and
and
* Fire Area 9: screenhouse, elevation 590'. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan.
* Fire Area 9: screenhouse, elevation 590.
 
The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.
 
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event.
 
Using the documents listed in the Attachment to this report, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP.


The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.
Documents reviewed are listed in the Attachment to this report.


Using the documents listed in the Attachment to this report, the inspectors verified that 6 fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP. Documents reviewed are listed in the Attachment to this report. These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.
These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.


====b. Findings====
====b. Findings====
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* utilization of pre-planned strategies;
* utilization of pre-planned strategies;
* adherence to the pre-planned drill scenario; and
* adherence to the pre-planned drill scenario; and
* drill objectives. Documents reviewed are listed in the Attachment to this report. These activities constituted one annual fire protection inspection sample as defined in IP 71111.05-05.
* drill objectives.
 
Documents reviewed are listed in the Attachment to this report.
 
These activities constituted one annual fire protection inspection sample as defined in IP 71111.05-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R06}}
 
7
{{a|1R06}}
==1R06 Flooding==
==1R06 Flooding==
{{IP sample|IP=IP 71111.06}}
{{IP sample|IP=IP 71111.06}}
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed selected risk-important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors reviewed flood analyses and design documents, including the UFSAR, engineering calculations, and abnormal operating procedures to identify licensee commitments. The inspectors also reviewed the licensee's corrective action documents with respect to past flood-related items identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following plant areas to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and were operable, and that the licensee complied with its commitments:
The inspectors reviewed selected risk-important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors reviewed flood analyses and design documents, including the UFSAR, engineering calculations, and abnormal operating procedures to identify licensee commitments. The inspectors also reviewed the licensees corrective action documents with respect to past flood-related items identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following plant areas to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and were operable, and that the licensee complied with its commitments:
* Service water pump screenhouse. Documents reviewed during this inspection are listed in the Attachment to this report. This inspection constituted one internal flooding sample as defined in IP 71111.06-05. Because the licensee reported finding several hundred gallons of water, some of which covered cables in Manhole 4, the inspectors elected to also perform an underground cable vaults inspection sample. This inspection sample is documented in Section 1R06.2.
* Service water pump screenhouse.
 
Documents reviewed during this inspection are listed in the Attachment to this report.
 
This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
 
Because the licensee reported finding several hundred gallons of water, some of which covered cables in Manhole 4, the inspectors elected to also perform an underground cable vaults inspection sample. This inspection sample is documented in Section 1R06.2.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected underground bunkers/manholes subject to flooding that contained cables whose failure could disable risk-significant equipment. The inspectors determined whether the cables were submerged, whether splices were intact, and whether appropriate cable support structures were in place. In those areas where dewatering devices were used, such as a sump pump, the inspectors determined whether the device was operable and level alarm circuits were set appropriately to ensure that the cables would not be submerged. In those areas without dewatering devices, the inspectors verified that drainage of the area was available, or that the cables were qualified for submerged conditions. The inspectors also reviewed the licensee's corrective action documents with respect to past submerged cable issues identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following underground bunkers/manholes subject to flooding:
The inspectors selected underground bunkers/manholes subject to flooding that contained cables whose failure could disable risk-significant equipment. The inspectors determined whether the cables were submerged, whether splices were intact, and whether appropriate cable support structures were in place. In those areas where dewatering devices were used, such as a sump pump, the inspectors determined whether the device was operable and level alarm circuits were set appropriately to ensure that the cables would not be submerged. In those areas without dewatering devices, the inspectors verified that drainage of the area was available, or that the cables were qualified for submerged conditions. The inspectors also reviewed the licensees corrective action documents with respect to past submerged cable issues identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following underground bunkers/manholes subject to flooding:
* Manholes 1, 2, 3, and 4.
* Manholes 1, 2, 3, and 4.


8 Documents reviewed are listed in the Attachment to this report.
Documents reviewed are listed in the Attachment to this report.


This inspection constituted one underground vaults sample as defined in IP 71111.06-05.
This inspection constituted one underground vaults sample as defined in IP 71111.06-05.
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====a. Inspection Scope====
====a. Inspection Scope====
On August 22, 2017, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification training. The inspectors verified that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and that training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
On August 22, 2017, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification training. The inspectors verified that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and that training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
* licensed operator performance;
* licensed operator performance;
* crew's clarity and formality of communications;
* crews clarity and formality of communications;
* ability to take timely actions in the conservative direction;
* ability to take timely actions in the conservative direction;
* prioritization, interpretation, and verification of annunciator alarms;
* prioritization, interpretation, and verification of annunciator alarms;
Line 172: Line 196:
* oversight and direction from supervisors;
* oversight and direction from supervisors;
* group dynamics involved in crew performance; and
* group dynamics involved in crew performance; and
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly licensed operator requalification program simulator sample as defined in IP 71111.11-05.
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.
 
The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one quarterly licensed operator requalification program simulator sample as defined in IP 71111.11-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the overall pass/fail results of the Annual Operating Test administered by the licensee from February 27, 2017 through March 30, 2017, required by Title 10 of the Code of Federal Regulations (CFR) 55.59(a). The results were compared to the thresholds established in Inspection Manual Chapter (IMC) 0609, Appendix I, "Licensed Operator Requalification Significance Determination Process," to assess the overall adequacy of the licensee's licensed operator requalification training program to meet the requirements of 10 CFR 55.59. (02.02)9 This inspection constituted one annual licensed operator requalification examination results sample as defined in Inspection Procedure 71111.11-05.
The inspectors reviewed the overall pass/fail results of the Annual Operating Test administered by the licensee from February 27, 2017 through March 30, 2017, required by Title 10 of the Code of Federal Regulations (CFR) 55.59(a). The results were compared to the thresholds established in Inspection Manual Chapter (IMC) 0609, Appendix I, Licensed Operator Requalification Significance Determination Process, to assess the overall adequacy of the licensees licensed operator requalification training program to meet the requirements of 10 CFR 55.59. (02.02)
This inspection constituted one annual licensed operator requalification examination results sample as defined in Inspection Procedure 71111.11-05.


====a. Findings====
====a. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}
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The inspectors evaluated degraded performance issues involving the following risk-significant systems:
The inspectors evaluated degraded performance issues involving the following risk-significant systems:
* emergency DGs; and
* emergency DGs; and
* charging system. The inspectors reviewed events including those in which ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
* charging system.
 
The inspectors reviewed events including those in which ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
* implementing appropriate work practices;
* implementing appropriate work practices;
* identifying and addressing common cause failures;
* identifying and addressing common cause failures;
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* trending key parameters for condition monitoring;
* trending key parameters for condition monitoring;
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
* verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1). The inspector performed a quality review for the DGs, as discussed in IP 71111.12, Section 02.02. The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly maintenance effectiveness sample and one quality control sample as defined in IP 71111.12-05.
* verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1).
 
The inspector performed a quality review for the DGs, as discussed in IP 71111.12, Section 02.02.
 
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one quarterly maintenance effectiveness sample and one quality control sample as defined in IP 71111.12-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
 
10
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
Line 216: Line 249:
* Emergent work on the control rod secondary position indication system concurrent with LS-1453, 1-2 DG fuel oil day tank level switch, modification;
* Emergent work on the control rod secondary position indication system concurrent with LS-1453, 1-2 DG fuel oil day tank level switch, modification;
* emergent troubleshooting and repairs to ESR1 & ESR2, 1-1 DG engine start relays; and
* emergent troubleshooting and repairs to ESR1 & ESR2, 1-1 DG engine start relays; and
* increased plant risk for planned 1-2 DG overspeed trip test, diving activities, and emergent door 15 (part of the control room heating, ventilation and air conditioning boundary) repairs. These activities were selected based on their potential risk significance relative to the Reactor Safety cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents reviewed during this inspection are listed in the Attachment to this report. These maintenance risk assessments and emergent work control activities constituted three samples as defined in IP 71111.13-05.
* increased plant risk for planned 1-2 DG overspeed trip test, diving activities, and emergent door 15 (part of the control room heating, ventilation and air conditioning boundary) repairs.
 
These activities were selected based on their potential risk significance relative to the Reactor Safety cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
 
Documents reviewed during this inspection are listed in the Attachment to this report.
 
These maintenance risk assessments and emergent work control activities constituted three samples as defined in IP 71111.13-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
{{a|1R15}}
==1R15 Operability Determinations and Functional Assessments==
==1R15 Operability Determinations and Functional Assessments==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}
Line 230: Line 268:
* immediate operability of 1-1 DG after failure of CV-0884B, 1-1 DG service water inlet valve, to close.
* immediate operability of 1-1 DG after failure of CV-0884B, 1-1 DG service water inlet valve, to close.


11 The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to the licensee's evaluations to determine
The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.


whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the Attachment to this report. This operability inspection constituted two samples as defined in IP 71111.15-05.
This operability inspection constituted two samples as defined in IP 71111.15-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
Line 247: Line 284:
* left channel load sequencer surveillance testing after replacement;
* left channel load sequencer surveillance testing after replacement;
* functional testing of RPS breaker after replacement; and
* functional testing of RPS breaker after replacement; and
* test start of 'B' charging pump after troubleshooting and emergent maintenance of baffle packing and adjusters. These activities were selected based upon the SSC's ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test  
* test start of B charging pump after troubleshooting and emergent maintenance of baffle packing and adjusters.
 
These activities were selected based upon the SSCs ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted five post-maintenance testing samples as defined in IP 71111.19-05.


documentation was properly evaluated. The inspectors evaluated the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to 12 determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report. This inspection constituted five post-maintenance testing samples as defined in IP 71111.19-05. b. (Open) Unresolved Item: Left Train Emergency Diesel Generator Load Sequencer Failure
b. (Open) Unresolved Item: Left Train Emergency Diesel Generator Load Sequencer Failure


=====Introduction:=====
=====Introduction:=====
Line 255: Line 296:


=====Description:=====
=====Description:=====
On August 3, 2017, the control room received alarm EK-1145, "Sequencer Trouble," unexpectedly. The operators identified that the indication lights were not lit on the left channel load sequencer, MC-34L101; declared the associated DG inoperable; and entered the appropriate TS action statement. The failed sequencer was removed and replaced with a new module that was satisfactorily post-maintenance tested and the left train EDG was subsequently declared operable on August 4, 2017. The failed sequencer was sent to an on-site lab for further troubleshooting. No obvious visual signs of failure were identified and the electrolytic capacitors in the module all tested satisfactorily. The module was then bench tested using a test program, which identified that although it would power up, no program would run. The licensee completed an equipment failure evaluation to review the bench test data, along with information collected in the failure modes analysis, and determined that the direct cause of the failure was a memory fault within the sequencer module that caused the sequencer to lock-up and not run its program. A fault in the memory module, memory processing interface circuitry, or the executive module could have caused the sequencer to lock up. At the end of the inspection period, further examination by the vendor was required and in progress to determine the exact initiating point of the fault. In addition to replacing the failed sequencer, the licensee's immediate corrective actions included inspecting the right train load sequencer and completing the quarterly surveillance test to ensure proper operation; the results of which were satisfactory. A plant operating experience review was conducted and did not identify any prior memory failures on the load sequencers. Once the vendor's evaluation is complete, the licensee plans to re-assess the failure mechanism and any additional corrective actions required. This item is considered unresolved, pending the inspectors' review of the vendor analysis and any changes made to the equipment failure evaluation, to determine if this issue constitutes a performance deficiency and/or violation of NRC requirements.
On August 3, 2017, the control room received alarm EK-1145, Sequencer Trouble, unexpectedly. The operators identified that the indication lights were not lit on the left channel load sequencer, MC-34L101; declared the associated DG inoperable; and entered the appropriate TS action statement. The failed sequencer was removed and replaced with a new module that was satisfactorily post-maintenance tested and the left train EDG was subsequently declared operable on August 4, 2017.
 
The failed sequencer was sent to an on-site lab for further troubleshooting. No obvious visual signs of failure were identified and the electrolytic capacitors in the module all tested satisfactorily. The module was then bench tested using a test program, which identified that although it would power up, no program would run. The licensee completed an equipment failure evaluation to review the bench test data, along with information collected in the failure modes analysis, and determined that the direct cause of the failure was a memory fault within the sequencer module that caused the sequencer to lock-up and not run its program. A fault in the memory module, memory processing interface circuitry, or the executive module could have caused the sequencer to lock up. At the end of the inspection period, further examination by the vendor was required and in progress to determine the exact initiating point of the fault.


(URI 05000255/2017003-01, Left Train Emergency Diesel Generator Load
In addition to replacing the failed sequencer, the licensees immediate corrective actions included inspecting the right train load sequencer and completing the quarterly surveillance test to ensure proper operation; the results of which were satisfactory. A plant operating experience review was conducted and did not identify any prior memory failures on the load sequencers. Once the vendors evaluation is complete, the licensee plans to re-assess the failure mechanism and any additional corrective actions required.


Sequencer Failure)
This item is considered unresolved, pending the inspectors review of the vendor analysis and any changes made to the equipment failure evaluation, to determine if this issue constitutes a performance deficiency and/or violation of NRC requirements.


13 c. (Open) Unresolved Item: Failure Mechanism of 42-2/RPS Reactor Protection System Breaker Failure to Open  
  (URI 05000255/2017003-01, Left Train Emergency Diesel Generator Load Sequencer Failure)c. (Open) Unresolved Item: Failure Mechanism of 42-2/RPS Reactor Protection System Breaker Failure to Open


=====Introduction:=====
=====Introduction:=====
Line 267: Line 310:


=====Description:=====
=====Description:=====
On May 17, 2017, the licensee conducted a shutdown to complete emergent repairs to a leaking seal identified on control rod drive mechanism 40. In accordance with GOP-8, "Power Reduction and Plant Shutdown to Mode 2 or Mode 3 525°F," the operators depressed the reactor trip pushbutton from the EC-06, reactor protection system panel. When the pushbutton was depressed, the reactor did not trip as expected. The operators successfully tripped the reactor using the reactor trip pushbutton on the EC-02, primary process and reactor controls console. The licensee identified that the 42-1/RPS breaker tripped as expected when the reactor trip pushbutton on the EC-06 panel was depressed, however, the 42-2/RPS breaker did not trip as expected. This resulted in the reactor trip not occurring as expected when the reactor trip pushbutton on the EC-06 panel was depressed as both breakers are required to open to result in a reactor trip.
On May 17, 2017, the licensee conducted a shutdown to complete emergent repairs to a leaking seal identified on control rod drive mechanism 40. In accordance with GOP-8, Power Reduction and Plant Shutdown to Mode 2 or Mode 3 525°F, the operators depressed the reactor trip pushbutton from the EC-06, reactor protection system panel. When the pushbutton was depressed, the reactor did not trip as expected. The operators successfully tripped the reactor using the reactor trip pushbutton on the EC-02, primary process and reactor controls console. The licensee identified that the 42-1/RPS breaker tripped as expected when the reactor trip pushbutton on the EC-06 panel was depressed, however, the 42-2/RPS breaker did not trip as expected. This resulted in the reactor trip not occurring as expected when the reactor trip pushbutton on the EC-06 panel was depressed as both breakers are required to open to result in a reactor trip.
 
The licensee performed troubleshooting activities to determine the cause of the  42-2/RPS breaker failure. The direct cause of the breaker failure was found to be the 42-2/RPS breaker undervoltage release mechanism failing to provide enough downward force to fully depress the trip plunger. This resulted in a physical failure of the breaker to open. At the end of the inspection period, the cause of this physical failure mode was unknown. The licensee's equipment failure evaluation identified that it could be age-related degradation or a physical degradation of the breaker. As a corrective action, a failure analysis of the breaker was planned. Once the failure analysis is complete, the licensee plans to re-assess the failure mechanism and determine any additional corrective actions that are required to address the issue. This item is considered unresolved, pending the inspectors' review of the failure analysis and any changes made to the equipment failure evaluation, to determine if this issue constitutes a performance deficiency and/or violation of NRC requirements.


(URI 05000255/2017003-02, Cause of 42-2/Reactor Protection System Breaker Failure to Open)
The licensee performed troubleshooting activities to determine the cause of the 42-2/RPS breaker failure. The direct cause of the breaker failure was found to be the 42-2/RPS breaker undervoltage release mechanism failing to provide enough downward force to fully depress the trip plunger. This resulted in a physical failure of the breaker to open. At the end of the inspection period, the cause of this physical failure mode was unknown. The licensees equipment failure evaluation identified that it could be age-related degradation or a physical degradation of the breaker. As a corrective action, a failure analysis of the breaker was planned. Once the failure analysis is complete, the licensee plans to re-assess the failure mechanism and determine any additional corrective actions that are required to address the issue. This item is considered unresolved, pending the inspectors review of the failure analysis and any changes made to the equipment failure evaluation, to determine if this issue constitutes a performance deficiency and/or violation of NRC requirements. (URI 05000255/2017003-02, Cause of 42-2/Reactor Protection System Breaker Failure to Open)
{{a|1R22}}
{{a|1R22}}
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
Line 278: Line 319:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural  
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
 
and TS requirements:
* RE-135, battery charger No. 3 performance test (routine);
* RE-135, battery charger No. 3 performance test (routine);
* RT-191, low power physics testing (routine);
* RT-191, low power physics testing (routine);
* QO-21A, 'A' auxiliary feedwater surveillance (inservice test); and
* QO-21A, A auxiliary feedwater surveillance (inservice test); and
* reactor coolant system (RCS) leak rate surveillance (RCS leak rate test).
* reactor coolant system (RCS) leak rate surveillance (RCS leak rate test).


14 The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:
The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:
* did preconditioning occur;
* did preconditioning occur;
* were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
* were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
Line 304: Line 343:
* was the reference setting data accurately incorporated into the test procedure;
* was the reference setting data accurately incorporated into the test procedure;
* was equipment returned to a position or status required to support the performance of its safety functions following testing;
* was equipment returned to a position or status required to support the performance of its safety functions following testing;
* were problems identified during the testing appropriately documented and dispositioned in the licensee's CAP;
* were problems identified during the testing appropriately documented and dispositioned in the licensees CAP;
* were annunciators and other alarms demonstrated to be functional and were setpoints consistent with design requirements; and
* were annunciators and other alarms demonstrated to be functional and were setpoints consistent with design requirements; and
* were alarm response procedure entry points and actions consistent with the plant design and licensing documents. This inspection constituted two routine surveillance testing samples, one in-service test sample, and one reactor coolant system leak detection inspection sample, as defined in IP 71111.22, Sections-02 and-05.
* were alarm response procedure entry points and actions consistent with the plant design and licensing documents.
 
This inspection constituted two routine surveillance testing samples, one in-service test sample, and one reactor coolant system leak detection inspection sample, as defined in IP 71111.22, Sections-02 and-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1EP2}}
 
15
{{a|1EP2}}
==1EP2 Alert and Notification System Evaluation==
==1EP2 Alert and Notification System Evaluation==
{{IP sample|IP=IP 71114.02}}
{{IP sample|IP=IP 71114.02}}
Line 318: Line 356:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed documents, and conducted discussions with Emergency Preparedness (EP) staff and management regarding the operation, maintenance, and periodic testing of the back-up and primary Alert and Notification System (ANS) in Palisade Nuclear Plant's plume pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and the daily and monthly operability records from July 2015 through July 2017. Information gathered during document reviews and interviews was used to determine whether the ANS equipment was maintained and tested in accordance with Emergency Plan commitments and procedures. Documents reviewed are listed in the Attachment to this report. This ANS inspection constituted one sample as defined in IP 71114.02
The inspectors reviewed documents, and conducted discussions with Emergency Preparedness (EP) staff and management regarding the operation, maintenance, and periodic testing of the back-up and primary Alert and Notification System (ANS) in Palisade Nuclear Plants plume pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and the daily and monthly operability records from July 2015 through July 2017. Information gathered during document reviews and interviews was used to determine whether the ANS equipment was maintained and tested in accordance with Emergency Plan commitments and procedures. Documents reviewed are listed in the Attachment to this report.
 
This ANS inspection constituted one sample as defined in IP 71114.02


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1EP3}}
{{a|1EP3}}
==1EP3 Emergency Response Organization Staffing and Augmentation System==
==1EP3 Emergency Response Organization Staffing and Augmentation System==
{{IP sample|IP=IP 71114.03}}
{{IP sample|IP=IP 71114.03}}
Line 328: Line 367:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed and discussed with plant EP management and staff the emergency plan commitments and procedures that addressed the primary and alternate methods of initiating an Emergency Response Organization (ERO) activation to augment the on-shift staff as well as the provisions for maintaining the plant's ERO team and qualification lists. The inspectors reviewed reports and a sample of CAP records of unannounced off-hour augmentation drills and call-in tests, which were conducted from July 2015 through July 2017, to determine the adequacy of the drill critiques and associated corrective actions. The inspectors also reviewed a sample of the training records of approximately 15 ERO personnel who were assigned to key and support positions, to determine the status of their training as it related to their assigned ERO positions. Documents reviewed are listed in the Attachment to this report. This ERO augmentation testing inspection constituted one sample as defined in IP 71114.03.
The inspectors reviewed and discussed with plant EP management and staff the emergency plan commitments and procedures that addressed the primary and alternate methods of initiating an Emergency Response Organization (ERO) activation to augment the on-shift staff as well as the provisions for maintaining the plants ERO team and qualification lists. The inspectors reviewed reports and a sample of CAP records of unannounced off-hour augmentation drills and call-in tests, which were conducted from July 2015 through July 2017, to determine the adequacy of the drill critiques and associated corrective actions. The inspectors also reviewed a sample of the training records of approximately 15 ERO personnel who were assigned to key and support positions, to determine the status of their training as it related to their assigned ERO positions. Documents reviewed are listed in the Attachment to this report.
 
This ERO augmentation testing inspection constituted one sample as defined in IP 71114.03.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1EP5}}
 
16
{{a|1EP5}}
==1EP5 Maintenance of Emergency Preparedness==
==1EP5 Maintenance of Emergency Preparedness==
{{IP sample|IP=IP 71114.05}}
{{IP sample|IP=IP 71114.05}}
Line 340: Line 378:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a sample of nuclear oversight staff audits of the EP Program to determine whether these independent assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and samples of CAP records associated with the 2016 biennial exercise, as well as various EP drills conducted in 2015, 2016 and 2017 to determine whether the licensee fulfilled drill commitments and to evaluate the licensee's efforts to identify, track, and resolve issues identified during these activities. The inspectors reviewed a sample of EP items and corrective actions related to the licensee's EP Program and activities to determine whether corrective actions were completed in accordance with the site's CAP. Documents reviewed are listed in the Attachment to this report. This correction of EP weaknesses and deficiencies inspection constituted one sample as defined in IP 71114.05.
The inspectors reviewed a sample of nuclear oversight staff audits of the EP Program to determine whether these independent assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and samples of CAP records associated with the 2016 biennial exercise, as well as various EP drills conducted in 2015, 2016 and 2017 to determine whether the licensee fulfilled drill commitments and to evaluate the licensees efforts to identify, track, and resolve issues identified during these activities. The inspectors reviewed a sample of EP items and corrective actions related to the licensee's EP Program and activities to determine whether corrective actions were completed in accordance with the sites CAP.
 
Documents reviewed are listed in the Attachment to this report.
 
This correction of EP weaknesses and deficiencies inspection constituted one sample as defined in IP 71114.05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1EP6}}
{{a|1EP6}}
==1EP6 Drill Evaluation==
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}
{{IP sample|IP=IP 71114.06}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the conduct of a routine licensee EP drill on August 16, 2017, to identify any weaknesses or deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the control room simulator, technical support center, and operations support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the CAP. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report. This emergency preparedness drill inspection constituted one sample as defined in IP 71114.06-06.
The inspectors evaluated the conduct of a routine licensee EP drill on August 16, 2017, to identify any weaknesses or deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the control room simulator, technical support center, and operations support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the CAP. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report.
 
This emergency preparedness drill inspection constituted one sample as defined in IP 71114.06-06.


====b. Findings====
====b. Findings====
Line 358: Line 401:
==2RS1 Radiological Hazard Assessment and Exposure Controls==
==2RS1 Radiological Hazard Assessment and Exposure Controls==
{{IP sample|IP=IP 71124.01}}
{{IP sample|IP=IP 71124.01}}
===.1 High Radiation Area and Very High Radiation Area Controls (02.06)
===.1 High Radiation Area and Very High Radiation Area Controls (02.06)===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed the controls for high radiation areas (HRAs) greater than 1 rem/hour and areas with the potential to become high radiation areas greater than 1 rem/hour for compliance with TSs and procedures. These inspection activities supplemented those documented in IR 05000255/2017002 and constituted a complete sample as defined in IP 71124.01-05.
The inspectors assessed the controls for high radiation areas (HRAs) greater than 1 rem/hour and areas with the potential to become high radiation areas greater than 1 rem/hour for compliance with TSs and procedures.
 
These inspection activities supplemented those documented in IR 05000255/2017002 and constituted a complete sample as defined in IP 71124.01-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|2RS5}}
{{a|2RS5}}
==2RS5 Radiation Monitoring Instrumentation==
==2RS5 Radiation Monitoring Instrumentation==
===
{{IP sample|IP=IP 71124.05}}
{{IP sample|IP=IP 71124.05}}
===.1 Walkdowns and Observations (02.02)===
===.1 Walkdowns and Observations (02.02)===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed select portable survey instruments that were available for use for current calibration and source check stickers, and instrument material condition and operability. The inspectors observed licensee staff dem onstrate performance checks of various types of portable survey instruments. The inspectors assessed whether high-range instruments responded to radiation on all appropriate scales. The inspectors walked down area radiation monitors and continuous air monitors to determine whether they were appropriately positioned relative to the radiation sources or areas they were intended to monitor. The inspectors compared monitor response with actual area conditions for selected monitors. The inspectors assessed the functional checks for select personnel contamination monitors, portal monitors, and small article monitors to verify they were performed in accordance with the manufacturer's recommendations and licensee procedures. These inspection activities constituted one complete sample as defined in IP 71124.05-05.
The inspectors assessed select portable survey instruments that were available for use for current calibration and source check stickers, and instrument material condition and operability.
 
The inspectors observed licensee staff demonstrate performance checks of various types of portable survey instruments. The inspectors assessed whether high-range instruments responded to radiation on all appropriate scales.
 
The inspectors walked down area radiation monitors and continuous air monitors to determine whether they were appropriately positioned relative to the radiation sources or areas they were intended to monitor. The inspectors compared monitor response with actual area conditions for selected monitors.
 
The inspectors assessed the functional checks for select personnel contamination monitors, portal monitors, and small article monitors to verify they were performed in accordance with the manufacturers recommendations and licensee procedures.
 
These inspection activities constituted one complete sample as defined in IP 71124.05-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
18


===.2 Calibration and Testing Program (02.03)===
===.2 Calibration and Testing Program (02.03)===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed laboratory analytical instruments used for radiological analyses to determine whether daily performance checks and calibration data indicated that the frequency of the calibrations was adequate and there were no indications of degraded  
The inspectors assessed laboratory analytical instruments used for radiological analyses to determine whether daily performance checks and calibration data indicated that the frequency of the calibrations was adequate and there were no indications of degraded instrument performance. The inspectors assessed whether appropriate corrective actions were implemented in response to indications of degraded instrument performance.
 
The inspectors reviewed the methods and sources used to perform whole body count functional checks before daily use and assessed whether check sources were appropriate and aligned with the plants isotopic mix. The inspectors reviewed whole body count calibration records since the last inspection and evaluated whether calibration sources were representative of the plant source term and that appropriate calibration phantoms were used. The inspectors looked for anomalous results or other indications of instrument performance problems.


instrument performance. The inspectors assessed whether appropriate corrective actions were implemented in response to indications of degraded instrument performance. The inspectors reviewed the methods and sources used to perform whole body count functional checks before daily use and assessed whether check sources were appropriate and aligned with the plant's isotopic mix. The inspectors reviewed whole body count calibration records since the last inspection and evaluated whether calibration sources were representative of the plant source term and that appropriate calibration phantoms were used. The inspectors looked for anomalous results or other indications of instrument performance problems. The inspectors reviewed select containment high-range monitor calibration and assessed whether an electronic calibration was completed for all range decades, with at least one decade at or below 10 rem/hour calibrated using an appropriate radiation source, and calibration acceptance criteria was reasonable. The inspectors reviewed select monitors used to survey personnel and equipment for unrestricted release to assess whether the alarm setpoints were reasonable under the circumstances to ensure that licensed material was not released from the site. The inspectors reviewed the calibration documentation for each instrument selected and discussed the calibration methods with the licensee to determine consistency with the manufacturer's recommendations. The inspectors reviewed calibration documentation for select portable survey instruments, area radiation monitors, and air samplers. The inspectors reviewed detector measurement geometry and calibration methods for portable survey instruments and area radiation monitors calibrated onsite and observed the licensee demonstrate use of the instrument calibrator. The inspectors assessed whether appropriate corrective actions were taken for instruments that failed performance checks or were found significantly out of calibration, and whether the licensee had evaluated the possible consequences of instrument use since the last successful calibration or performance check. The inspectors reviewed the current output values for instrument calibrators. The inspectors assessed whether the licensee periodically measured calibrator output over the range of the instruments used with measuring devices that had been calibrated by a facility using National Institute of Standards and Technology traceable sources and whether corrective factors for these measuring devices were properly applied in its output verification. The inspectors reviewed the licensee's 10 CFR Part 61, "Licensing Requirements for Land Disposal of Radioactive Waste," source term to assess whether calibration sources used were representative of the types and energies of radiation encountered in the plant.
The inspectors reviewed select containment high-range monitor calibration and assessed whether an electronic calibration was completed for all range decades, with at least one decade at or below 10 rem/hour calibrated using an appropriate radiation source, and calibration acceptance criteria was reasonable.


19 These inspection activities constituted one complete sample as defined in IP 71124.05-05.
The inspectors reviewed select monitors used to survey personnel and equipment for unrestricted release to assess whether the alarm setpoints were reasonable under the circumstances to ensure that licensed material was not released from the site. The inspectors reviewed the calibration documentation for each instrument selected and discussed the calibration methods with the licensee to determine consistency with the manufacturers recommendations.
 
The inspectors reviewed calibration documentation for select portable survey instruments, area radiation monitors, and air samplers. The inspectors reviewed detector measurement geometry and calibration methods for portable survey instruments and area radiation monitors calibrated onsite and observed the licensee demonstrate use of the instrument calibrator. The inspectors assessed whether appropriate corrective actions were taken for instruments that failed performance checks or were found significantly out of calibration, and whether the licensee had evaluated the possible consequences of instrument use since the last successful calibration or performance check.
 
The inspectors reviewed the current output values for instrument calibrators. The inspectors assessed whether the licensee periodically measured calibrator output over the range of the instruments used with measuring devices that had been calibrated by a facility using National Institute of Standards and Technology traceable sources and whether corrective factors for these measuring devices were properly applied in its output verification.
 
The inspectors reviewed the licensees 10 CFR Part 61, Licensing Requirements for Land Disposal of Radioactive Waste, source term to assess whether calibration sources used were representative of the types and energies of radiation encountered in the plant.
 
These inspection activities constituted one complete sample as defined in IP 71124.05-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated whether problems associated with radiation monitoring instrumentation were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involved radiation monitoring instrumentation. These inspection activities constituted one complete sample as defined in IP 71124.05-05.
The inspectors evaluated whether problems associated with radiation monitoring instrumentation were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involved radiation monitoring instrumentation.
 
These inspection activities constituted one complete sample as defined in IP 71124.05-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|2RS6}}
{{a|2RS6}}
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
{{IP sample|IP=IP 71124.06}}
{{IP sample|IP=IP 71124.06}}
Line 405: Line 464:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors walked down select effluent radiation monitoring systems to evaluate whether the monitor configurations aligned with Offsite Dose Calculation Manual (ODCM) descriptions and to observe the material condition of the systems. The inspectors walked down selected components of the gaseous and liquid discharge systems to evaluate whether equipment configuration and flow paths aligned with plant documentation and to assess equipment material condition. The inspectors also assessed whether there were potential unmonitored release points, building alterations which could impact effluent controls, and ventilation system leakage that communicated directly with the environment. For equipment or areas associated with the systems selected for review that were not readily accessible, the inspectors reviewed the licensee's material condition surveillance records. The inspectors walked down filtered ventilation systems to assess for conditions such as degraded high efficiency particulate air/charcoal banks, improper alignment, or system installation issues that would impact the performance or the effluent monitoring capability of the effluent system. As available, the inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluents to evaluate whether appropriate treatment equipment was used and the processing activities aligned with discharge permits.
The inspectors walked down select effluent radiation monitoring systems to evaluate whether the monitor configurations aligned with Offsite Dose Calculation Manual (ODCM) descriptions and to observe the material condition of the systems.
 
The inspectors walked down selected components of the gaseous and liquid discharge systems to evaluate whether equipment configuration and flow paths aligned with plant documentation and to assess equipment material condition. The inspectors also assessed whether there were potential unmonitored release points, building alterations which could impact effluent controls, and ventilation system leakage that communicated directly with the environment.


20 The inspectors determined if the licensee had made significant changes to their effluent release points. As available, the inspectors observed selected portions of the routine processing and discharging of liquid waste to determine if appropriate effluent treatment equipment was being used, and whether radioactive liquid waste was being processed and discharged in accordance with procedure requirements and aligned with discharge permits. These inspection activities constituted one complete sample as defined in IP 71124.06-05.
For equipment or areas associated with the systems selected for review that were not readily accessible, the inspectors reviewed the licensee's material condition surveillance records.
 
The inspectors walked down filtered ventilation systems to assess for conditions such as degraded high efficiency particulate air/charcoal banks, improper alignment, or system installation issues that would impact the performance or the effluent monitoring capability of the effluent system.
 
As available, the inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluents to evaluate whether appropriate treatment equipment was used and the processing activities aligned with discharge permits.
 
The inspectors determined if the licensee had made significant changes to their effluent release points.
 
As available, the inspectors observed selected portions of the routine processing and discharging of liquid waste to determine if appropriate effluent treatment equipment was being used, and whether radioactive liquid waste was being processed and discharged in accordance with procedure requirements and aligned with discharge permits.
 
These inspection activities constituted one complete sample as defined in IP 71124.06-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed calibration and functional tests for select effluent monitors to evaluate whether they were performed consistent with the ODCM. The inspectors assessed whether National Institute of Standards and Technology traceable sources were used, primary calibration represented the plant nuclide mix, secondary calibrations verified the primary calibration, and calibration encompassed the alarm setpoints. The inspectors assessed whether effluent monitor alarm setpoints were established as provided in the ODCM and procedures. The inspectors evaluated the basis for changes to effluent monitor alarm setpoints.
The inspectors reviewed calibration and functional tests for select effluent monitors to evaluate whether they were performed consistent with the ODCM. The inspectors assessed whether National Institute of Standards and Technology traceable sources were used, primary calibration represented the plant nuclide mix, secondary calibrations verified the primary calibration, and calibration encompassed the alarm setpoints.
 
The inspectors assessed whether effluent monitor alarm setpoints were established as provided in the ODCM and procedures.
 
The inspectors evaluated the basis for changes to effluent monitor alarm setpoints.


These inspection activities constituted one complete sample as defined in IP 71124.06-05.
These inspection activities constituted one complete sample as defined in IP 71124.06-05.
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed select effluent sampling activities and assessed whether adequate controls had been implemented to ensure representative samples were obtained. The inspectors reviewed select effluent discharges made with inoperable effluent radiation monitors and assessed whether controls were in place to ensure compensatory sampling was performed consistent with the ODCM and that those controls were adequate to prevent the release of unmonitored effluents. The inspectors determined whether the facility was routinely relying on the use of compensatory sampling in lieu of adequate system maintenance.
The inspectors reviewed select effluent sampling activities and assessed whether adequate controls had been implemented to ensure representative samples were obtained.


21 The inspectors reviewed the results of the inter-laboratory comparison program to evaluate the quality of the radioactive effluent sample analyses and assessed whether the inter-laboratory comparison program included hard-to-detect isotopes as appropriate. These inspection activities constituted one complete sample as defined in IP 71124.06-05.
The inspectors reviewed select effluent discharges made with inoperable effluent radiation monitors and assessed whether controls were in place to ensure compensatory sampling was performed consistent with the ODCM and that those controls were adequate to prevent the release of unmonitored effluents.
 
The inspectors determined whether the facility was routinely relying on the use of compensatory sampling in lieu of adequate system maintenance.
 
The inspectors reviewed the results of the inter-laboratory comparison program to evaluate the quality of the radioactive effluent sample analyses and assessed whether the inter-laboratory comparison program included hard-to-detect isotopes as appropriate.
 
These inspection activities constituted one complete sample as defined in IP 71124.06-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the methodology used to determine the effluent stack and vent flow rates to determine if the flow rates were consistent with plant documentation, and whether differences between assumed and actual stack and vent flow rates affected the results of the projected public dose. The inspectors assessed whether surveillance test results for TS required ventilation effluent discharge systems met TS acceptance criteria. The inspectors assessed calibration and availability for select effluent monitors used for triggering emergency action levels or for determining protective action recommendations. These inspection activities constituted one complete sample as defined in IP 71124.06-05.
The inspectors reviewed the methodology used to determine the effluent stack and vent flow rates to determine if the flow rates were consistent with plant documentation, and whether differences between assumed and actual stack and vent flow rates affected the results of the projected public dose.
 
The inspectors assessed whether surveillance test results for TS required ventilation effluent discharge systems met TS acceptance criteria.
 
The inspectors assessed calibration and availability for select effluent monitors used for triggering emergency action levels or for determining protective action recommendations.
 
These inspection activities constituted one complete sample as defined in IP 71124.06-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed significant changes in reported dose values compared to the previous radiological effluent release report to evaluate the factors which may have resulted in the change. The inspectors reviewed radioactive liquid and gaseous waste discharge permits to assess whether the projected dose to members of the public were accurate. The inspectors evaluated the isotopes included in the source term to assess whether analysis methods were sufficient to satisfy detectability standards. The review included the current Part 61 analyses to ensure hard-to-detect radionuclides were included in the source term. The inspectors reviewed changes in the licensee's offsite dose calculations and evaluated whether those changes were consistent with the ODCM and Regulatory 22 Guide 1.109. The inspectors reviewed meteorological dispersion and deposition factors used in the ODCM and effluent dose calculations and determined whether appropriate factors were being used for public dose calculations. The inspectors reviewed the latest Land Use Census to assess whether changes had been factored into the dose calculations. For select radioactive waste discharges, the inspectors evaluated whether the calculated doses were within the 10 CFR, Part 50, Appendix I and TS dose criteria. The inspectors reviewed select records of abnormal radioactive waste discharges to ensure the discharges were monitored by the discharge point effluent monitor. Discharges made with inoperable effluent radiation monitors, or unmonitored leakages were reviewed to ensure that an evaluation was made to account for the source term and projected dose to the public. These inspection activities constituted one complete sample as defined in IP 71124.06-05.
The inspectors reviewed significant changes in reported dose values compared to the previous radiological effluent release report to evaluate the factors which may have resulted in the change.
 
The inspectors reviewed radioactive liquid and gaseous waste discharge permits to assess whether the projected dose to members of the public were accurate.
 
The inspectors evaluated the isotopes included in the source term to assess whether analysis methods were sufficient to satisfy detectability standards. The review included the current Part 61 analyses to ensure hard-to-detect radionuclides were included in the source term.
 
The inspectors reviewed changes in the licensees offsite dose calculations and evaluated whether those changes were consistent with the ODCM and Regulatory Guide 1.109. The inspectors reviewed meteorological dispersion and deposition factors used in the ODCM and effluent dose calculations and determined whether appropriate factors were being used for public dose calculations.
 
The inspectors reviewed the latest Land Use Census to assess whether changes had been factored into the dose calculations.
 
For select radioactive waste discharges, the inspectors evaluated whether the calculated doses were within the 10 CFR, Part 50, Appendix I and TS dose criteria.
 
The inspectors reviewed select records of abnormal radioactive waste discharges to ensure the discharges were monitored by the discharge point effluent monitor.
 
Discharges made with inoperable effluent radiation monitors, or unmonitored leakages were reviewed to ensure that an evaluation was made to account for the source term and projected dose to the public.
 
These inspection activities constituted one complete sample as defined in IP 71124.06-05.


====b. Findings====
====b. Findings====
Line 451: Line 554:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed whether problems associated with the effluent monitoring and control program were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. In addition, the inspectors evaluated the appropriateness of the corrective actions for a selected sample of problems documented by the licensee involving radiation monitoring and exposure controls. These inspection activities constituted one complete sample as defined in IP 71124.06-05.
The inspectors assessed whether problems associated with the effluent monitoring and control program were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. In addition, the inspectors evaluated the appropriateness of the corrective actions for a selected sample of problems documented by the licensee involving radiation monitoring and exposure controls.
 
These inspection activities constituted one complete sample as defined in IP 71124.06-05.


====b. Findings====
====b. Findings====
Line 457: Line 562:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
Line 464: Line 569:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Drill/Exercise Performance (DEP) performance indicator (PI) for the period from the second quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, were used. The inspectors reviewed the licensee's records associated with the PI to verify that the licensee accurately reported the DEP indicator in accordance with relevant procedures and the NEI guidance. Specifically, the inspectors reviewed licensee records and processes, including procedural guidance on assessing opportunities for the PI; assessments of PI opportunities during pre-designated control room simulator training sessions; performance during the 2016 biennial exercise; and performance during other drills. Specific documents reviewed are listed in the Attachment to this report.
The inspectors sampled licensee submittals for the Drill/Exercise Performance (DEP)performance indicator (PI) for the period from the second quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the DEP indicator in accordance with relevant procedures and the NEI guidance. Specifically, the inspectors reviewed licensee records and processes, including procedural guidance on assessing opportunities for the PI; assessments of PI opportunities during pre-designated control room simulator training sessions; performance during the 2016 biennial exercise; and performance during other drills. Specific documents reviewed are listed in the Attachment to this report.


This inspection constitutes one DEP sample as defined in IP 71151.
This inspection constitutes one DEP sample as defined in IP 71151.
Line 474: Line 579:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the ERO Drill Participation PI for the period from the second quarter of 2016 through the second quarter of 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, were used. The inspectors reviewed the licensee's records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures, and NEI guidance. Specifically, the inspectors reviewed licensee records and processes, including procedural guidance on assessing opportunities for the PI; performance during the 2016 biennial exercise; and other drills; and revisions of the roster of personnel assigned to key ERO positions. Specific documents reviewed are listed in the Attachment to this report. This inspection constitutes one ERO drill participation sample as defined in IP 71151.
The inspectors sampled licensee submittals for the ERO Drill Participation PI for the period from the second quarter of 2016 through the second quarter of 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures, and NEI guidance. Specifically, the inspectors reviewed licensee records and processes, including procedural guidance on assessing opportunities for the PI; performance during the 2016 biennial exercise; and other drills; and revisions of the roster of personnel assigned to key ERO positions. Specific documents reviewed are listed in the Attachment to this report.
 
This inspection constitutes one ERO drill participation sample as defined in IP 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
24


===.3 Alert and Notification System Reliability===
===.3 Alert and Notification System Reliability===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the ANS PI for the period from the second quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, were used. The inspectors reviewed the licensee's records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures and the NEI Guidance. Specifically, the inspectors reviewed licensee records and processes including procedural guidance on assessing opportunities for the PI and results of periodic ANS operability tests. Specific documents reviewed are listed in the Attachment to this report. This inspection constitutes one ANS sample as defined in IP 71151.
The inspectors sampled licensee submittals for the ANS PI for the period from the second quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures and the NEI Guidance. Specifically, the inspectors reviewed licensee records and processes including procedural guidance on assessing opportunities for the PI and results of periodic ANS operability tests. Specific documents reviewed are listed in the Attachment to this report.
 
This inspection constitutes one ANS sample as defined in IP 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.4 Mitigating Systems Performance Index-High Pressure Injection System===
===.4 Mitigating Systems Performance IndexHigh Pressure Injection System===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - High Pressure Injection System PI for the period from the third quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensee's operator narrative logs, CRs, MSPI derivation reports, event reports and NRC Integrated IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report. This inspection constituted one MSPI high pressure injection system sample as defined in IP 71151-05.
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - High Pressure Injection System PI for the period from the third quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, event reports and NRC Integrated IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one MSPI high pressure injection system sample as defined in IP 71151-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.5 Mitigating Systems Performance Index-Residual Heat Removal System===
===.5 Mitigating Systems Performance IndexResidual Heat Removal System===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System PI for the period from the third quarter 2016 through the second quarter 2017.
The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System PI for the period from the third quarter 2016 through the second quarter 2017.


25 To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensee's operator narrative logs, CRs, MSPI derivation reports, event reports and NRC IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report. This inspection constituted one MSPI residual heat removal system sample as defined in IP 71151-05.
To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, event reports and NRC IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one MSPI residual heat removal system sample as defined in IP 71151-05.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals for the RCS Leakage PI for the period from the third quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensee's operator  
The inspectors sampled licensee submittals for the RCS Leakage PI for the period from the third quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, RCS leakage tracking data, CRs, event reports and NRC IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.


narrative logs, RCS leakage tracking data, CRs, event reports and NRC IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report. This inspection constituted one reactor coolant system leakage sample as defined in IP 71151-05.
This inspection constituted one reactor coolant system leakage sample as defined in IP 71151-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA2}}
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
Line 522: Line 632:


====a. Inspection Scope====
====a. Inspection Scope====
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensee's corrective action program at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensee's 26 corrective action program as a result of the inspectors' observations; however, they are not discussed in this report. These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter.
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees corrective action program at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensees corrective action program as a result of the inspectors observations; however, they are not discussed in this report.
 
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Annual Follow-up of Selected Issues:===
===.2 Annual Follow-up of Selected Issues: 1-2 Diesel Generator Issues Resulting in===
1-2 Diesel Generator Issues Resulting in Additional Inoperability
 
Additional Inoperability


====a. Inspection Scope====
====a. Inspection Scope====
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* CR-PLP-2017-00609, Received Alarm EK-0555, Diesel Generator Breaker 152-213 Trip, Unexpectedly;
* CR-PLP-2017-00609, Received Alarm EK-0555, Diesel Generator Breaker 152-213 Trip, Unexpectedly;
* CR-PLP-2017-01291, While Performing MO-7A-2, Breaker 152-213 Opened and K-6B, Emergency Diesel Generator 1-2, Tripped; and
* CR-PLP-2017-01291, While Performing MO-7A-2, Breaker 152-213 Opened and K-6B, Emergency Diesel Generator 1-2, Tripped; and
* CR-PLP-2017-02655, Failure of P-18A to Shutoff at the Desired Setpoint. Between January 2017 and July 2017, the licensee initiated multiple condition reports involving the 1-2 DG for issues that resulted in additional inoperability of the system.
* CR-PLP-2017-02655, Failure of P-18A to Shutoff at the Desired Setpoint.
 
Between January 2017 and July 2017, the licensee initiated multiple condition reports involving the 1-2 DG for issues that resulted in additional inoperability of the system.
 
The inspectors reviewed these condition reports and their associated work orders.


The inspectors reviewed these condition reports and their associated work orders. As appropriate, the inspectors verified the following attributes during their review of the licensee's corrective actions for the above condition reports and other related condition reports:
As appropriate, the inspectors verified the following attributes during their review of the licensee's corrective actions for the above condition reports and other related condition reports:
* complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
* complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
* consideration of the extent of condition, generic implications, common cause, and previous occurrences;
* consideration of the extent of condition, generic implications, common cause, and previous occurrences;
Line 544: Line 661:
* identification of corrective actions, which were appropriately focused to correct the problem;
* identification of corrective actions, which were appropriately focused to correct the problem;
* completion of corrective actions in a timely manner commensurate with the safety significance of the issue; and
* completion of corrective actions in a timely manner commensurate with the safety significance of the issue; and
* evaluation of the applicability for operating experience and communication of applicable lessons learned to appropriate organizations. The inspectors discussed the corrective actions and associated evaluations with licensee personnel. This review constituted one in-depth problem identification and resolution inspection sample as defined in IP 71152.
* evaluation of the applicability for operating experience and communication of applicable lessons learned to appropriate organizations.
 
The inspectors discussed the corrective actions and associated evaluations with licensee personnel.
 
This review constituted one in-depth problem identification and resolution inspection sample as defined in IP 71152.
 
b. Observations and Assessments The inspectors reviewed the adverse condition analyses (ACA) associated with CR-PLP-2017-00609 and CR-PLP-2017-02655, and the disposition associated with CR-PLP-2017-01291. The inspectors did not identify any significant issues associated with the licensees CAP processes for these condition reports. However, the inspectors noted the licensees conclusions in the ACA associated with CR-PLP-2017-02655.
 
The licensees ACA for the issue identified in CR-PLP-2017-02655, which occurred on May 23, 2017, discussed previous occurrences of similar failures. On May 23, 2017, during performance a monthly surveillance test on the 1-2 DG, the P-18A fuel oil transfer pump would not stop auto-filling the 1-2 DG fuel oil day tank. The licensee manually stopped the pump and, although the 1-2 DG was already inoperable due to the surveillance test, declared the 1-2 DG inoperable due to the P-18A auto-fill function not operating as expected. The licensee performed troubleshooting and identified that LS-1453, the 1-2 DG fuel oil day tank low level switch, contacts did not open as expected when sufficient level in the 1-2 DG fuel oil day tank was reached. As a result of this condition, the P-18A fuel oil transfer pump did not stop auto-filling as anticipated.
 
Through troubleshooting the licensee identified that the probable cause was binding due to air entrapment of the level switch float in the upper portion of the float chamber. The resulting actions were to adjust the level switch mechanism to prevent air entrapment in LS-1453.


27 b. Observations and Assessments The inspectors reviewed the adverse condition analyses (ACA) associated with  CR-PLP-2017-00609 and CR-PLP-2017-02655, and the disposition associated with CR-PLP-2017-01291. The inspectors did not identify any significant issues associated with the licensee's CAP processes for these condition reports. However, the inspectors noted the licensee's conclusions in the ACA associated with CR-PLP-2017-02655. The licensee's ACA for the issue identified in CR-PLP-2017-02655, which occurred on May 23, 2017, discussed previous occurrences of similar failures. On May 23, 2017, during performance a monthly surveillance test on the 1-2 DG, the P-18A fuel oil transfer pump would not stop auto-filling the 1-2 DG fuel oil day tank. The licensee manually stopped the pump and, although the 1-2 DG was already inoperable due to the surveillance test, declared the 1-2 DG inoperable due to the P-18A auto-fill function not operating as expected. The licensee performed troubleshooting and identified that LS-1453, the 1-2 DG fuel oil day tank low level switch, contacts did not open as expected when sufficient level in the 1-2 DG fuel oil day tank was reached. As a result of this condition, the P-18A fuel oil transfer pump did not stop auto-filling as anticipated.
The ACA discussed similar failures of level switch LS-1453 that had occurred on four other occasions since 2013. An apparent cause evaluation (ACE) was performed for one of these failures on May 18, 2015. In this case, when the automatic fill function for the 1-2 DG fuel oil day tank was placed into service, P-18A started to fill the tank, even though tank level was sufficient and the operators expected P-18A to remain off. The licensee determined the cause of the event to be contact between the level switch and a seismic support for the tank, which resulted in binding due to a misalignment of the internal float in LS-1453. Additionally, it was discussed in the ACE that, due to the contact, the level switch and associated piping was not plumb. This was identified as a legacy issue associated with inadequate understanding of the impact of interference when the level switch was installed. For this event, the level switch internals were modified to eliminate the binding. Additionally, a corrective action was created to evaluate rework of the piping for the level switch and eliminate the contact with the seismic support. It was decided that the piping rework was an enhancement action and no active rework of the piping was pursued.


Through troubleshooting the licensee identified that the probable cause was binding due to air entrapment of the level switch float in the upper portion of the float chamber. The resulting actions were to adjust the level switch mechanism to prevent air entrapment in LS-1453. The ACA discussed similar failures of level switch LS-1453 that had occurred on four other occasions since 2013. An apparent cause evaluation (ACE) was performed for one of these failures on May 18, 2015. In this case, when the automatic fill function for the 1-2 DG fuel oil day tank was placed into service, P-18A started to fill the tank, even though tank level was sufficient and the operators expected P-18A to remain off. The licensee determined the cause of the event to be contact between the level switch and a seismic support for the tank, which resulted in binding due to a misalignment of the internal float in LS-1453. Additionally, it was discussed in the ACE that, due to the contact, the level switch and associated piping was not plumb. This was identified as a legacy issue associated with inadequate understanding of the impact of interference when the level switch was installed. For this event, the level switch internals were modified to eliminate the binding. Additionally, a corrective action was created to evaluate rework of the piping for the level switch and eliminate the contact with the seismic support. It was decided that the piping rework was an enhancement action and no active rework of the piping was pursued. Two of the similar failures occurred in January 2017 and April 2017. In each of these instances, the licensee identified possible failure mechanisms and implemented corrective actions to restore operability. However, the licensee determined, for these events, that there were several possible causes that could not be eliminated through the troubleshooting process. The ACA identified that corrective actions in the previous  
Two of the similar failures occurred in January 2017 and April 2017. In each of these instances, the licensee identified possible failure mechanisms and implemented corrective actions to restore operability. However, the licensee determined, for these events, that there were several possible causes that could not be eliminated through the troubleshooting process. The ACA identified that corrective actions in the previous events did not adequately eliminate the identified possible failure mechanisms. The identified possible failure mechanisms were mitigated, but not eliminated completely.


events did not adequately eliminate the identified possible failure mechanisms. The identified possible failure mechanisms were mitigated, but not eliminated completely.
The inspectors noted that the ACA also discussed that rework of the level switch piping, which was identified as an enhancement in 2015, would eliminate all possible causes.


The inspectors noted that the ACA also discussed that rework of the level switch piping, which was identified as an enhancement in 2015, would eliminate all possible causes. The licensee's corrective action to rework the level switch piping and replace LS-1453 was completed on July 28, 2017. This resulted in the assurance that the level switch 28 piping was plumb and the contact between LS-1453 and the seismic support was eliminated.
The licensees corrective action to rework the level switch piping and replace LS-1453 was completed on July 28, 2017. This resulted in the assurance that the level switch piping was plumb and the contact between LS-1453 and the seismic support was eliminated.


====c. Findings====
====c. Findings====


=====Introduction:=====
=====Introduction:=====
A finding of very low safety significance (Green) and an associated non-cited violation (NCV) of TS 5.4.1, "Procedures", was self-revealed on March 31, 2017, when the 1-2 DG tripped during performance of monthly TS surveillance procedure MO-7A-2, "Emergency Diesel Generator 1-2.Specifically, during conduct of the monthly surveillance procedure, restoration activities associated with maintenance of breaker 152-213, 1-2 DG to Bus 1D, were being performed. When maintenance personnel closed the trip cutouts for the Z-phase of the 1-2 DG differential overcurrent relay, an unbalanced current flow into the differential relay resulted in relay actuation. This actuation resulted in a trip of the output breaker and subsequently a trip of the 1-2 DG. The trip caused a delay in the TS surveillance activities, and resulted in extended unavailability and inoperability of the 1-2 DG.
A finding of very low safety significance (Green) and an associated non-cited violation (NCV) of TS 5.4.1, Procedures, was self-revealed on March 31, 2017, when the 1-2 DG tripped during performance of monthly TS surveillance procedure MO-7A-2, Emergency Diesel Generator 1-2. Specifically, during conduct of the monthly surveillance procedure, restoration activities associated with maintenance of breaker 152-213, 1-2 DG to Bus 1D, were being performed. When maintenance personnel closed the trip cutouts for the Z-phase of the 1-2 DG differential overcurrent relay, an unbalanced current flow into the differential relay resulted in relay actuation. This actuation resulted in a trip of the output breaker and subsequently a trip of the 1-2 DG. The trip caused a delay in the TS surveillance activities, and resulted in extended unavailability and inoperability of the 1-2 DG.


=====Description:=====
=====Description:=====
On March 31, 2017, the monthly TS surveillance procedure for the 1-2 DG was scheduled to start at 12:00 p.m. The preventive maintenance associated with the 1-2 DG differential overcurrent relay was scheduled to end at 1:00 p.m. This indicated to operators that these work activities were not bound by any logic tie and the activities could be overlapped. When maintenance personnel performing the maintenance activities associated with the relay work identified that the 1-2 DG was running, they requested permission from the control room to place the Z-phase differential relay back into service prior to closing breaker 152-213, 1-2 DG to Bus 1D output breaker. The operators informed the maintenance personnel that they could return the relay to service when breaker 152-213 was closed. Once breaker 152-213 was closed during the surveillance procedure, the maintenance workers were restoring the relay when it tripped, causing breaker 152-213 and the 1-2 DG to trip. The maintenance personnel immediately informed the control room of their activities and promptly revealed the cause of the DG trip. This sequence of events caused additional inoperability and unavail ability time of the 1-2 DG due to time taken for evaluation of the trip and re-performing the surveillance test. Prior to the start of the surveillance test, the licensee had declared the 1-2 DG inoperable and appropriately entered TS 3.8.1, Condition B. The licensee restored the differential overcurrent trip relay circuitry and successfully re-performed the test. Once those activities were completed, the DG was declared operable. As discussed in the licensee's disposition evaluation for this issue, this event was directly caused by restoration of the differential relay while the DG output breaker was closed. The engineering staff identified that the differential relay properly actuated as designed, which resulted in the trip of the 1-2 DG. As corrective actions, the licensee updated work instructions associated with the differential overcurrent relays to include caution statements that opening or closing trip cutouts for the differential relays while the output breakers from the DGs to the associated buses were closed could cause the differential relays to actuate.
On March 31, 2017, the monthly TS surveillance procedure for the 1-2 DG was scheduled to start at 12:00 p.m. The preventive maintenance associated with the 1-2 DG differential overcurrent relay was scheduled to end at 1:00 p.m. This indicated to operators that these work activities were not bound by any logic tie and the activities could be overlapped.
 
When maintenance personnel performing the maintenance activities associated with the relay work identified that the 1-2 DG was running, they requested permission from the control room to place the Z-phase differential relay back into service prior to closing breaker 152-213, 1-2 DG to Bus 1D output breaker. The operators informed the maintenance personnel that they could return the relay to service when breaker 152-213 was closed. Once breaker 152-213 was closed during the surveillance procedure, the maintenance workers were restoring the relay when it tripped, causing breaker 152-213 and the 1-2 DG to trip. The maintenance personnel immediately informed the control room of their activities and promptly revealed the cause of the DG trip. This sequence of events caused additional inoperability and unavailability time of the 1-2 DG due to time taken for evaluation of the trip and re-performing the surveillance test. Prior to the start of the surveillance test, the licensee had declared the 1-2 DG inoperable and appropriately entered TS 3.8.1, Condition B. The licensee restored the differential overcurrent trip relay circuitry and successfully re-performed the test. Once those activities were completed, the DG was declared operable.
 
As discussed in the licensees disposition evaluation for this issue, this event was directly caused by restoration of the differential relay while the DG output breaker was closed. The engineering staff identified that the differential relay properly actuated as designed, which resulted in the trip of the 1-2 DG. As corrective actions, the licensee updated work instructions associated with the differential overcurrent relays to include caution statements that opening or closing trip cutouts for the differential relays while the output breakers from the DGs to the associated buses were closed could cause the differential relays to actuate.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that the failure to adequately pre-plan and perform maintenance that could affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate 29 to the circumstances was contrary to the requirements of TS 5.4.1, "Procedures", and was a performance deficiency warranting further review. The performance deficiency was determined to be more than minor, and thus a finding, in accordance with IMC 0612, Appendix B, "Issue Screening," dated September 7, 2012, because it was associated with the Mitigating Systems cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined the finding could be evaluated using the Significance Determination Process in accordance with IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," Exhibit 2, dated June 19, 2012. The inspectors reviewed the Mitigating Systems Screening Questions in Appendix A, Exhibit 2 and answered "No" to all questions. As a result, the finding was determined to be very of low safety significance (Green). This finding had a cross-cutting aspect in the area of Human Performance, in the Work Management aspect, for the failure to identify and manage risk commensurate to the work. Specifically, the licensee committed a human performance error by failing to adequately plan, control, and execute electrical maintenance activities associated with the 1-2 DG during the monthly TS surveillance test of the DG. The licensee did not appropriately assess and coordinate the work activities of different work groups to address the impact of those work activities on the plant, which resulted in the 1-2 DG being inoperable longer than planned (H.5).
The inspectors determined that the failure to adequately pre-plan and perform maintenance that could affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances was contrary to the requirements of TS 5.4.1, Procedures, and was a performance deficiency warranting further review.
 
The performance deficiency was determined to be more than minor, and thus a finding, in accordance with IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, because it was associated with the Mitigating Systems cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
 
The inspectors determined the finding could be evaluated using the Significance Determination Process in accordance with IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, dated June 19, 2012. The inspectors reviewed the Mitigating Systems Screening Questions in Appendix A, Exhibit 2 and answered No to all questions. As a result, the finding was determined to be very of low safety significance (Green).
 
This finding had a cross-cutting aspect in the area of Human Performance, in the Work Management aspect, for the failure to identify and manage risk commensurate to the work. Specifically, the licensee committed a human performance error by failing to adequately plan, control, and execute electrical maintenance activities associated with the 1-2 DG during the monthly TS surveillance test of the DG. The licensee did not appropriately assess and coordinate the work activities of different work groups to address the impact of those work activities on the plant, which resulted in the 1-2 DG being inoperable longer than planned (H.5).


=====Enforcement:=====
=====Enforcement:=====
Line 570: Line 707:
NRC Regulatory Guide 1.33, Appendix A, Section 9a, states, in part, that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.
NRC Regulatory Guide 1.33, Appendix A, Section 9a, states, in part, that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.


Contrary to the above, on March 31, 2017, while performing monthly TS surveillance procedure MO-7A-2, "Emergency Diesel Generator 1-2," in conjunction with electrical maintenance procedure WI-SPS-E-09, "Calibration of Bus 1D Protective Relays," the licensee failed to properly pre-plan and perform maintenance that affected the 1-2 DG by failing to understand the impact of restoration of the Z-phase differential overcurrent relay while the 1-2 DG output breaker was closed. Specifically, performance of these two activities in conjunction with each other resulted in unbalanced current flow into the differential relay and a trip of the 1-2 DG. The issue was entered into the licensee's CAP as CR-PLP-2017-01291, While Performing MO-7A-2, Breaker 152-213 Opened and K-6B, Emergency Diesel Generator 1-2, Tripped. Because this violation was of very low safety significance and it was entered into the licensee's CAP as CR-PLP-2017-01291, this violation is being treated as a NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000255/2017003-03, 1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG)
Contrary to the above, on March 31, 2017, while performing monthly TS surveillance procedure MO-7A-2, Emergency Diesel Generator 1-2, in conjunction with electrical maintenance procedure WI-SPS-E-09, Calibration of Bus 1D Protective Relays, the licensee failed to properly pre-plan and perform maintenance that affected the 1-2 DG by failing to understand the impact of restoration of the Z-phase differential overcurrent relay while the 1-2 DG output breaker was closed. Specifically, performance of these two activities in conjunction with each other resulted in unbalanced current flow into the differential relay and a trip of the 1-2 DG. The issue was entered into the licensees CAP as CR-PLP-2017-01291, While Performing MO-7A-2, Breaker 152-213 Opened and K-6B, Emergency Diesel Generator 1-2, Tripped.
 
Because this violation was of very low safety significance and it was entered into the licensees CAP as CR-PLP-2017-01291, this violation is being treated as a NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.


30
(NCV 05000255/2017003-03, 1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG)
{{a|4OA3}}
{{a|4OA3}}
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
{{IP sample|IP=IP 71153}}
{{IP sample|IP=IP 71153}}
===.1 (Closed) Licensee Event Report===
===.1 (Closed) Licensee Event Report 05000255/2017002-00: Reactor Protection System===
 
Actuation While the Reactor was Shutdown On May 19, 2017, an unexpected actuation of the RPS occurred during the performance of procedure PO-1, Operations Pre-Startup Tests. While testing the function of RPS actuation from a loss of main generator load input signal, the operator performing the test incorrectly determined MOD-389, the Main Generator Motor-Operated Disconnect, to be open when it was actually closed. The PO-1 procedure required that either MOD-389 be in the open position or that the main generator protective trip circuitry be bypassed. Because the operator incorrectly determined the state of the motor-operated disconnect, the aforementioned conditional step was erroneously performed, and the main generator protective trip circuitry was not bypassed as required, leading to the unplanned RPS actuation. At the time of the actuation, the reactor was shutdown in Mode 5 with all control rods inserted and the RPS responded as expected for the plant conditions. The operator was given remediation training and enhancements to procedure guidance were briefed to all operating crews on the execution of conditional steps. Also, the licensee increased required behavioral observations and supervisory oversight within the operations department.


05000255/2017002-00:  Reactor Protection System Actuation While the Reactor was Shutdown On May 19, 2017, an unexpected actuation of the RPS occurred during the performance of procedure PO-1, "Operations Pre-Startup Tests."  While testing the function of RPS actuation from a loss of main generator load input signal, the operator performing the test incorrectly determined MOD-389, the Main Generator Motor-Operated Disconnect, to be open when it was actually closed. The PO-1 procedure required that either  MOD-389 be in the open position or that the main generator protective trip circuitry be bypassed. Because the operator incorrectly determined the state of the motor-operated disconnect, the aforementioned conditional step was erroneously performed, and the main generator protective trip circuitry was not bypassed as required, leading to the unplanned RPS actuation. At the time of the actuation, the reactor was shutdown in Mode 5 with all control rods inserted and the RPS responded as expected for the plant conditions. The operator was given remediation training and enhancements to procedure guidance were briefed to all operating crews on the execution of conditional steps. Also, the licensee increased required behavioral observations and supervisory oversight within the operations department. The inspectors determined that the failure of the operator to correctly perform procedure PO-1, "Operations Pre-Startup Tests," constituted a performance deficiency and that this performance deficiency was similar to Example 4.b of IMC 0612, Appendix E, "Examples of Minor Issues.For this issue, the unexpected RPS actuation produced a valid RPS signal for a reactor trip. However, the trip did not result in any upset to plant stability since control rods were fully inserted due to the plant being shutdown.
The inspectors determined that the failure of the operator to correctly perform procedure PO-1, Operations Pre-Startup Tests, constituted a performance deficiency and that this performance deficiency was similar to Example 4.b of IMC 0612, Appendix E, Examples of Minor Issues. For this issue, the unexpected RPS actuation produced a valid RPS signal for a reactor trip. However, the trip did not result in any upset to plant stability since control rods were fully inserted due to the plant being shutdown.


Therefore, the failure to follow the RPS testing procedure constituted a minor violation that is not subject to enforcement action in accordance with the NRC's Enforcement Policy. This licensee event report (LER) is closed.
Therefore, the failure to follow the RPS testing procedure constituted a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. This licensee event report (LER) is closed.


Documents reviewed are listed in the Attachment to this report.
Documents reviewed are listed in the Attachment to this report.


This event follow-up review constituted one sample as defined in IP 71153-05.
This event follow-up review constituted one sample as defined in IP 71153-05.
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Management Meetings==
==4OA6 Management Meetings==


===.1 Exit Meeting Summary On October 18, 2017, the inspectors presented the inspection results to Mr. C. Arnone, Site Vice President, and other members of the licensee staff.===
===.1 Exit Meeting Summary===
The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.
 
On October 18, 2017, the inspectors presented the inspection results to Mr. C. Arnone, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.
 
===.2 Interim Exit Meetings===


===.2 Interim Exit Meetings Interim exits were conducted for:===
Interim exits were conducted for:
* the inspection results of the Emergency Preparedness Program with Mr. C. Arnone, Site Vice President, and licensee staff on July 20, 2017; and
* the inspection results of the Emergency Preparedness Program with Mr. C. Arnone, Site Vice President, and licensee staff on July 20, 2017; and
* the inspection results for the Radiation Safety Program review with Mr. D. Corbin, General Manager Plant Operations, and licensee staff on July 14, 2017.
* the inspection results for the Radiation Safety Program review with Mr. D. Corbin, General Manager Plant Operations, and licensee staff on July 14, 2017.


31 The inspectors confirmed that none of the potential report input discussed was considered proprietary. Proprietary material received during the inspection was returned to the licensee.
The inspectors confirmed that none of the potential report input discussed was considered proprietary. Proprietary material received during the inspection was returned to the licensee.
 
{{a|4OA7}}
{{a|4OA7}}
==4OA7 Licensee-Identified Violations The following licensee-identified violation of U.S. Nuclear Regulatory Commission requirements was determined to be of very low safety significance or Severity Level IV and meet the U.S. Nuclear Regulatory Commission Enforcement Policy criteria for being==
==4OA7 Licensee-Identified Violations==
 
The following licensee-identified violation of U.S. Nuclear Regulatory Commission requirements was determined to be of very low safety significance or Severity Level IV and meet the U.S. Nuclear Regulatory Commission Enforcement Policy criteria for being dispositioned as a Non-Cited Violation.
* The licensee identified a finding of very low safety significance (Green) and an associated NCV of TS 5.7.2, which requires, in part, that each entryway into High Radiation Areas (HRAs) with dose rates greater than 1.0 rem/hour at 30 centimeters from the radiation source or any surface penetrated by the radiation, but less than 500 rads/hour at 1 meter from the radiation source or from any surface penetrated by the radiation source shall be provided with a locked or continuously guarded door or gate that prevents unauthorized entry. Contrary to the above, on May 4, 2017, the licensee failed to lock or continuously guard an entryway into a HRA with dose rates greater than 1.0 rem/hour at 30 centimeters from the radiation source or any surface penetrated by the radiation, but less than 500 rads/hour at 1 meter from the radiation source or from any surface penetrated by the radiation source. Specifically, an entryway was left unguarded when the individual assigned to guard the entryway left the area prior to another guard being stationed. This issue was identified by a radiation protection technician who immediately stationed another guard. This issue was entered into the licensees CAP as CR-PL-2017-02160.
 
The failure to continuously guard the HRA entryway was a performance deficiency that was within the licensees ability to foresee and should have been prevented. The performance deficiency was more than minor because it was associated with the Program and Process attribute of the Occupational Radiation Safety cornerstone and adversely affected the cornerstone objective of ensuring the adequate protection of worker health and safety from exposure to radiation.
 
The finding was determined to be of very low safety significance (Green)because it did not involve as-low-as-reasonably-achievable planning or work controls, there was no overexposure or substantial potential for an overexposure, and the licensees ability to assess dose was not compromised.


dispositioned as a Non-Cited Violation.
ATTACHMENT:  
* The licensee identified a finding of very low safety significance (Green) and an associated NCV of TS 5.7.2, which requires, in part, that each entryway into High Radiation Areas (HRAs) with dose rates greater than 1.0 rem/hour at 30 centimeters from the radiation source or any surface penetrated by the radiation, but less than 500 rads/hour at 1 meter from the radiation source or from any surface penetrated by the radiation source shall be provided with a locked or continuously guarded door or gate that prevents unauthorized entry. Contrary to the above, on May 4, 2017, the licensee failed to lock or continuously guard an entryway into a HRA with dose rates greater than 1.0 rem/hour at 30 centimeters from the radiation source or any surface penetrated by the radiation, but less than 500 rads/hour at 1 meter from the radiation source or from any surface penetrated by the radiation source. Specifically, an entryway was left unguarded when the individual assigned to guard the entryway left the area prior to another guard being stationed. This issue was identified by a radiation protection technician who immediately stationed another guard. This issue was entered into the licensee's CAP as CR-PL-2017-02160. The failure to continuously guard the HRA entryway was a performance deficiency that was within the licensee's ability to foresee and should have been prevented. The performance deficiency was more than minor because it was associated with the Program and Process attribute of the Occupational Radiation Safety cornerstone and adversely affected the cornerstone objective of ensuring the adequate protection of worker health and safety from exposure to radiation. The finding was determined to be of very low safety significance (Green)because it did not involve as-low-as-reasonably-achievable planning or work controls, there was no overexposure or substantial potential for an overexposure, and the licensee's ability to assess dose was not compromised. ATTACHMENT:


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 606: Line 758:
==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==


Licensee  
Licensee
: [[contact::C. Arnone]], Site Vice President  
: [[contact::C. Arnone]], Site Vice President
: [[contact::D. Corbin]], General Manager Plant Operations  
: [[contact::D. Corbin]], General Manager Plant Operations
: [[contact::B. Baker]], Operations Manager - Shift  
: [[contact::B. Baker]], Operations Manager - Shift
: [[contact::J. Borah]], Engineering Manager, Systems and Components  
: [[contact::J. Borah]], Engineering Manager, Systems and Components
: [[contact::T. Davis]], Regulatory Assurance  
: [[contact::T. Davis]], Regulatory Assurance
: [[contact::N. DeMaster]], Outage Manager  
: [[contact::N. DeMaster]], Outage Manager
: [[contact::B. Dotson]], Regulatory Assurance  
: [[contact::B. Dotson]], Regulatory Assurance
: [[contact::J. Erickson]], Regulatory Assurance  
: [[contact::J. Erickson]], Regulatory Assurance
: [[contact::O. Gustafson]], Director of Regulatory and Performance Improvement  
: [[contact::O. Gustafson]], Director of Regulatory and Performance Improvement
: [[contact::J. Hardy]], Regulatory Assurance Manager  
: [[contact::J. Hardy]], Regulatory Assurance Manager
: [[contact::J. Haumersen]], Site Projects and Maintenance Services Manager  
: [[contact::J. Haumersen]], Site Projects and Maintenance Services Manager
: [[contact::G. Heisterman]], Maintenance Manager  
: [[contact::G. Heisterman]], Maintenance Manager
: [[contact::K. Howard]], Emergency Preparedness Specialist  
: [[contact::K. Howard]], Emergency Preparedness Specialist
: [[contact::M. Lee]], Operations Manager - Support  
: [[contact::M. Lee]], Operations Manager - Support
: [[contact::D. Lucy]], Production Manager  
: [[contact::D. Lucy]], Production Manager
: [[contact::D. Malone]], Emergency Planning Manager  
: [[contact::D. Malone]], Emergency Planning Manager
: [[contact::T. Mulford]], Operations Manager  
: [[contact::T. Mulford]], Operations Manager
: [[contact::W. Nelson]], Training Manager  
: [[contact::W. Nelson]], Training Manager
: [[contact::D. Nestle]], Radiation Protection Manager
: [[contact::D. Nestle]], Radiation Protection Manager
: [[contact::C. Plachta]], Nuclear Independent Oversight Manager  
: [[contact::C. Plachta]], Nuclear Independent Oversight Manager
: [[contact::M. Mylnarek]], Nuclear Independent Oversight Manager  
: [[contact::M. Mylnarek]], Nuclear Independent Oversight Manager
: [[contact::K. O'Connor]], Site Engineering Director  
: [[contact::K. OConnor]], Site Engineering Director
: [[contact::M. Schultheis]], Performance Improvement Manager  
: [[contact::M. Schultheis]], Performance Improvement Manager
: [[contact::M. Soja]], Chemistry Manager  
: [[contact::M. Soja]], Chemistry Manager
: [[contact::J. Tharp]], Security Manager  
: [[contact::J. Tharp]], Security Manager
: [[contact::U.S. Nuclear Regulatory Commission E. Duncan]], Chief, Reactor Projects Branch 3
U.S. Nuclear Regulatory Commission
: [[contact::E. Duncan]], Chief, Reactor Projects Branch 3


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


===Opened===
===Opened===
: 05000255/2017003-01 URI Left Train Emergency Diesel Generator Load Sequencer
: 05000255/2017003-01   URI   Left Train Emergency Diesel Generator Load Sequencer Failure (Section 1R19.1.b)
Failure (Section 1R19.1.b)  
: 05000255/2017003-02   URI   Cause of 42-2/RPS Breaker Failure to Open (Section 1R19.1.c)
: 05000255/2017003-02 URI Cause of 42-2/RPS Breaker Failure to Open (Section 1R19.1.c)  
: 05000255/2017003-03   NCV   1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG (Section 4OA2.2.c)
: 05000255/2017003-03 NCV 1-2 Diesel Generator Trip During Maintenance Resulting
in Additional Unavailabili
ty of the 1-2 DG (Section
4OA2.2.c)  


===Closed===
===Closed===
: [[Closes LER::05000255/LER-2017-002]]-00 LER Reactor Protection System Actuation While the Reactor
: 05000255/2017002-00   LER   Reactor Protection System Actuation While the Reactor was Shutdown (Section 4OA3.1)
was Shutdown (Section 4OA3.1)
: 05000255/2017003-03   NCV   1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG (Section 4OA2.2.c)
: [[Closes finding::05000255/FIN-2017003-03]] NCV 1-2 Diesel Generator Trip During Maintenance Resulting
in Additional Unavailabili
ty of the 1-2 DG (Section  
: 4OA2.2.c)  


===Discussed===
===Discussed===


None    
None


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
The following is a partial list of documents reviewed during the inspection.
 
: Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort.
: Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
: 1R01 Adverse Weather Protection - Admin 4.00, Operations Organization, Responsibilities, and Conduct, Revision 62 - Admin 4.02, Control of Equipment, Revision 77
- Admin 4.28, Control of Palisades Switchyard Activities, Revision 9
-
: AOP-38, Acts of Nature Basis, Revision 9 -
: AOP-38, Acts of Nature, Revision 11 -
: CR-PLP-2017-04135, Entered
: AOP-38 "Acts of Nature" Due to a Geo-Magnetic Storm with a
: K Index of 7, September 7, 2017 -
: CR-PLP-2017-04142, The Corporate Duty Manager (CDM) was Not Informed Within Two Hours of an Unplanned Change in Risk Achievement Work (RAW), September 8, 2017 -
: CR-PLP-2017-04144, A Yellow Risk Level (RAW of 3.66) was Entered Unplanned Due to a Geomagnetic Storm, September 8, 2017 -
: EN-WM-104, On-Line Risk Assessment, Revision 15 - Operations Log, Thursday, September 7, 2017 1R04 Equipment Alignment -
: CR-PLP-2016-01434, Dry White Boric Acid Crystals on Component
: FI-0212 High Side Block Valve, March 23, 2016 -
: CR-PLP-2016-01794, An Accumulation of Boric Acid Crystals were Observed on
: MV-CVC507 Charging Pumps Pumped Feed Supply Line Bent, April 14, 2016 -
: CR-PLP-2016-01887, For Charging Pump P-55C There are Two Nuts at the Anchor Bolts on the South East Corner of the Pump, April 20, 2016 -
: CR-PLP-2016-02955,
: VOP-3009, HPSI to Reactor Coolant Loop 1B Valve Operator Main Gearbox and Motor Pinion Greases were Grade 3, June 28, 2016 -
: CR-PLP-2016-04514,
: MV-SW607 Service Water Pump P-7C Discharge Press Instrument Root Leaks by Approximately 10-20 mls a Second, September 23, 2016 -
: CR-PLP-2016-04597, Dry Boric Acid on the High Side Block Valve Stem on the Five Valve Block that
: FI-0212 is Attached to, September 28, 2016 -
: CR-PLP-2017-01806,
: MV-ES3188 HPSI PP P-66A Miniflow and
: MV-ES3179 HPSI Pump P-66B Miniflow were Found in the Locked Open Position when the Test Position is Locked Closed, April 25, 2017 -
: CR-PLP-2017-01923,
: FIC-0210A, Primary Makeup Water Flow Start Push-Button Requires Excessive Force for Dilution Initiation, April 28, 2017 -
: CR-PLP-2017-02838, Operations Devonway Performance Indicator (PI) 'Component Mispositioning' Turned Yellow, July 20, 2017 -
: CR-PLP-2017-03000, Noted that
: FI-0212 "Charging Pumps Local Flow Indicator" was Reading Less than 40 gpm while the Charging System was in Double Charging and Letdown, June 19, 2017 -
: CR-PLP-2017-03213, Operations Devonway Performance Indicator (PI) 'Component Mispositioning 6-Month Cumulative' Turned Red, July 5, 2017 
-
: CR-PLP-2017-04068, NRC Identified Compressed Air Manual Valve with No Label in Second Level Component Cooling Water, August 31, 2017 -
: CR-PLP-2017-04121, NPO Noticed Water on the Floor in the Boric Acid Tank Room, September 7, 2017 -
: CR-PLP-2017-04134, During a Tour of P-55A Charging Pump Bay, the NRC Resident Found
a Valve Located Near the Suction Side Flush Manifold that is Missing its Valve Label, September 7, 2017 - M-201, Piping & Instrument Diagram, Primary Coolant System, Sheet 1, Revision 90
- M-202, Piping & Instrument Diagram, Chemical & Volume Control System, Sheet 1B, Revision 60 - M-202, Piping & Instrument Diagram, Chemical & Volume Control System, Sheet 1A, Revision 64 - M-203, Piping & Instrument Diagram, Safety Injection, Containment Spray and Shutdown Cooling System, Sheet 2, Revision 28 - M-204, Piping & Instrument Diagram, Safety Injection Containment Spray and Shutdown Cooling System, Sheet 1A, Revision 44 - M-204, Piping & Instrument Diagram, Safety Injection Containment Spray and Shutdown Cooling System, Sheet 1, Revision 88 - M-204, Piping & Instrument Diagram, Safety Injection Containment Spray, Sheet 1B, Revision 41 - M-208, Piping & Instrument Diagram, Service Water System, Sheet 1A, Revision 65
- M-209, Piping & Instrument Diagram, Component Cooling System, Sheet 2, Revision 33
- M-213, Piping & Instrument Diagram, Service Water, Screen Structure and Chlorinator, Revision 96 -
: QO-19, Inservice Test Procedure - HPSI Pumps & ESS Check Valve Operability Test, Revision 42 -
: SOP-15, Service Water System, Revision 67
-
: SOP-2A, Chemical and Volume Control System, Revision 87
-
: SOP-2B, Chemical and Volume Control System, Purification and Chemical Injection, Revisions 52 and 53 -
: SOP-3, Safety Injection and Shutdown Cooling System, Revision 105 - Tagout Tag List, 1C26-1-CVC-016-01-2165, September 6, 2017 - Tagout Tag List, 1C26-2-CVC-008-MV-CVC2162, September 6, 2017 1R05 Fire Protection - 2017 Fire Drill Tracker -
: CR-PLP-2016-02873, Fire Tour Routes Differ Slightly Between Security Officers, June 22, 2016 -
: CR-PLP-2016-03599, Transient Combustible Evaluation 16-051 was Initiated Late for
: WO 52647942-2, August 2, 2016 -
: CR-PLP-2017-01880, Poor Housekeeping Identified on Turbine Building Walkdown, April 27, 2017 -
: CR-PLP-2017-03341, Door 35, Entrance to Screenhouse, was Found Open Upon Alarm Response by Security, July 13, 2017 -
: CR-PLP-2017-03362, Door 35 is not Staying Shut Within a Reasonable Time Limit Once Entering the Screenhouse, July 15, 2017 -
: CR-PLP-2017-03421, Compensatory Measure for Non-Exempt Combustibles in the Screen House was Not Recorded in the Operations Fire Tour/Fire Watch Log, July 18, 2017 -
: CR-PLP-2017-03465, Security Received an Alarm on Vital Area Door 35 and was Found Un-Secure Upon Response by Security, July 22, 2017 
-
: CR-PLP-2017-04187, Door 35, Screenhouse Entrance, was Found Closed but Not Latched Upon Alarm Response by Security, September 12, 2017 -
: CR-PLP-2017-04200, Observed Where Door-35, Screenhouse Laydown Area East Door has Re-Opened After Being Physically Challenged as a Close Fire/Security Door, September 12, 2017 -
: CR-PLP-2017-04204, Door 35, Entrance to Screenhouse was Found Unsecured Upon Alarm Response, September 13, 2017 -
: CR-PLP-2017-04256, During Fire Drill #32 it was Determined that Two Scott-75 SCBA Packs were Found Unusable by Fire Brigade Members, September 15, 2017 -
: CR-PLP-2017-04318, While Inspecting SCBA's after Fire Drill, One of the Air Packs was Tagged Out of Service, September 20, 2017 -
: CR-PLP-2017-04426, NIOS Identified:
: One Fire Brigade Member Improperly Donned the SCBA Mask, September 20, 2017 -
: CR-PLP-2017-04436,
: TS-1899, Cable Penetration Room South Exhaust Fan V-62 Ventilator is Not Functioning as Intended, September 28, 2017 -
: DBD-7.10, NFPA 805 Fire Protection Program, Revision 1
-
: EA-FPP-03-001, Analysis of Combustible Loading at Palisades Nuclear Plant, Revision 3 - EAL Basis, Emergency Action Level Technical Bases, Revision 7
-
: EM-09-24, Service Water and Fire Protection Inspection Program, Revision 3 -
: EN-DC-161, Control of Combustibles, Revisions 17 -
: EN-OP-139, Fire Watch Program, Revision 1
- Fire Tour/Fire Watch Log, September 6, 2017
-
: FPIP-2, Fire Emergency Responsibility and Response, Revision 23
-
: FPIP-4, Fire Protection Systems and Fire Protection Equipment, Revision 38
-
: LM-0311 Qualification Matrix, September 20, 2017 - M-216, Fire Protection System, Sheet 4, Revision 13 - Monthly SCBA Checklist, August 2017
- Monthly SCBA Checklist, December 2016
- Monthly SCBA Checklist, February 2017
- Monthly SCBA Checklist, May 2017 - Operations Logs, September 6, 2017 - Pre Fire Plan 26, Southwest Cable Penetration Room, Elevation 590' and 607'
- Pre Fire Plan 3, 1-D Switchgear Room & North Cableway, Elevation 607'
- Pre Fire Plan 9, Screenhouse, Elevation 590'
- Pre Fire Plans 5 & 7, Diesel Generator 1-1 and Fuel Oil Day Tank Room, Elevation 590'
- Pre Fire Plans 6 & 8, Diesel Generator 1-2 and Fuel Oil Day Tank Room, Elevation 590' -
: WO 419680, Door-35 Latching Mechanism Seems to be Sticking -
: WO 52752445, Respiratory Protection Equipment Inspection 1R06 Flood Protection Measures - Calculation
: EA-EC55593-01, Beyond Design Basis (BDB) Evaluation:
: Local Intense Precipitation Flow Through Manhole 4 to Manhole 1, February 19, 2015 -
: CR-PLP-2017-03068, During Manhole 4 Inspection there was a Significant Amount of Water in the Manhole (> 6 inches), June 23, 2017 - E-315, Embedded Conduit and Grounding Sections, Revision 15
- Entergy Letter to NRC,
: PNP 2015-018, Required Response 2 for Near-Term Task Force Recommendation 2.1:
: Flooding - Hazard Re-Evaluation Report, March 11, 2015 - Entergy Letter to NRC,
: PNP 2016-063, Mitigating Strategies Assessment for Flooding Submittal, December 19, 2016 
- NRC Letter to Entergy, Palisades Nuclear Plant - Interim Staff Response to Reevaluated Flood Hazards Submitted in Response to 10
: CFR 50.54(f) Information Request - Flood -
: Causing Mechanism Reevaluation (TAC No. MF6128), December 23, 2015 - Work Order
: 52745949, Manhole 4 - Submerged Cable Inspection, June 23, 2017 1R11 Licensed Operator Requalification Program -
: CR-PLP-2017-03827, During a Simulator Scenario Certain Valve Indications were Spiking to Full Scale and then Back to Zero, August 15, 2017 -
: CR-PLP-2017-03841, Simulator Crash Due to Microsoft Windows Issue, August 16, 2017 -
: PLSES-LOR-17B-CPE6, "Crew Performance Examination," Revision 5 1R12 Maintenance Effectiveness -
: CR-PLP-10`7-03206, P-55A, 'A' Charging Pump was Indicating up to 500 rpm, July 4, 2017 -
: CR-PLP-2015-03722, Seal Lube Tank for P-55B, 'B' Charging Pump had to be Refilled after Dropping to 55%, September 8, 2015 -
: CR-PLP-2016-02845, An Error was Identified in Engineering Report
: POP-RPT-16-00007 (Final Eddy Current Inspection Report, 1-1 K-6A, Emergency Diesel Generator), June 21, 2016 -
: CR-PLP-2016-03211, Three Key System Health Work Orders Were Not Prioritized Correctly, July 13, 2016 -
: CR-PLP-2016-03900, Lowering Pressurizer Level, August 22, 2016
-
: CR-PLP-2016-04534, PCS Leak on P-55B Charging Pump, September 25, 2016
-
: CR-PLP-2016-05007, The September 24, 2016 Charging Pump-P-55B Discharge Manifold Flush Line Leak has been Determined to be a Maintenance Rule Functional Failure, October 20, 2016 -
: CR-PLP-2016-05281, Recent Issues Affecting the Emergency Diesel Generators Should be Reviewed for Potential Aggregate Impact, November 3, 2016 -
: CR-PLP-2016-05531, K-6A, Emergency Diesel Generator 1-1, is Considered Near (a)(1), November 18, 2016 -
: CR-PLP-2016-05563, Over the Past Two Months there have been Three Identified Leaks on Jacket Water Hoses on K-6B, 1-2 Emergency Diesel Generator, November 21, 2016 -
: CR-PLP-2016-05566, Starting Air Pressure for the 'A' Train on the 1-2 Emergency Diesel Generator after Starting per
: MO-7A-2, Monthly Surveillance was 137 psig, November 21, 2016 -
: CR-PLP-2017-00387, Chemical and Volume Control System Health Report Turned Yellow Due to Charging Pumps P-55A, P-55B, and P-55C in Maintenance Rule (a)(1) Status, January 31, 2017 -
: CR-PLP-2017-00640, Leak on the Outlet of T-31D, EDG 1-2 K-6B Air Starting Tank, February 22, 2017 -
: CR-PLP-2017-00731, TM Installed for Breaker 52, 1308 with be Installed Beyond the Next Refueling Outage, February 28, 2017 -
: CR-PLP-2017-00950, K-6B, Emergency Diesel Generator 1-2, is Considered Near (a)(1) Due to Exceeding 75% of its Maintenance Rule Unavailability, March 15, 2017 -
: CR-PLP-2017-01296, Hanger JB24-H3, 14 ('A' Air Start Train Piping) Broke, April 1, 2017
-
: CR-PLP-2017-01316, Water Present in Oil Sample Drawn from Charging Pump P-55B, April 3, 2017 -
: CR-PLP-2017-01405, Attempt to Rack Out 52-1105, Charging Pump P-55C Breaker for Maintenance, April 7, 2017 -
: CR-PLP-2017-01418, Charging Pump P-55C Discharge Could Not be Operated Open per Restoration, April 7, 2017 
-
: CR-PLP-2017-01419, P-55A, 'A' Charging Pump, Failed to Start, April 8, 2017 -
: CR-PLP-2017-01422, Metal Shavings in Oil in Fluid Drive of Charging Pump P-55A, April 8, 2017 -
: CR-PLP-2017-01586, Shutter Mechanism is Bent Internal to the Breaker on Charging Pump Motor P-55B, April 19, 2017 -
: CR-PLP-2017-01588, Failure of Charging Pump P-55A Determined to be a Maintenance Rule Functional Failure, April 19, 2017 -
: CR-PLP-2017-01970, Could Not Get Charging Springs to Discharge While Removing Charging Pump P-55C Breaker, April 29, 2017 -
: CR-PLP-2017-02654, 1-2 Diesel Generator Jacket Water Hoses Noted to be Leaking, May 22, 2017 -
: CR-PLP-2017-02847,
: EMB-11-5, P-55C Offline Baker Test Resistance Status Delta R Failed, June 7, 2017 -
: CR-PLP-2017-02917, Received Alarm
: EK-0557 Unexpectedly, June 13, 2017 -
: CR-PLP-2017-02966, P-55C, 'C' Charging Pump is Making an Abnormal Noise, June 18, 2017 -
: CR-PLP-2017-03039, P-55C, 'C' Charging Pump Tripped Upon Second Start of Pump, June 21, 2017 -
: CR-PLP-2017-03076, P-55C Baker Test taken from 52-1105 PI did Not Pass the Minimum Tolerance Test, June 24, 2017 -
: CR-PLP-2017-03077, Removal of Switches 52-1105 A and B for P-55C, June 24, 2017 -
: CR-PLP-2017-03165, NIOS Observer Found a Broken 1/2" Bolt Lying on the Diesel Skid Near the Jacket Water Pump, June 30, 2017 -
: CR-PLP-2017-03179, Drawings do Not Match the Physical Configuration in the Field, June 30, 2017 -
: CR-PLP-2017-03221, Control Room Received Alarm
: EK-0557, Diesel Generator No. 1-2
: Trouble, Unexpectedly, July 5, 2017 -
: CR-PLP-2017-03253, Technician Could Not get the Low Raw Water Pressure Alarm (EK_3011, D/G 1-2 Low Raw Water Pressure) to Reset, July 7, 2017 -
: CR-PLP-2017-03263, Found the Exhaust Heat Shield East Side Upper Mounting Bolt Missing Just South of the Turbocharger on K-6B, July 8, 2017 -
: CR-PLP-2017-03276, RWPR Relay Appears to be Mechanically Bound and will Not Reposition, July 10, 2017 -
: CR-PLP-2017-03285, Removed Relay RWPR on 1-2 Emergency Diesel Generator per
: WO 47988855-03, July 10, 2017 -
: CR-PLP-2017-03290, During the Replacement of Relay G1-2/RWPR a Piece of Plastic Broke Off the New Relay, July 10, 2017 -
: CR-PLP-2017-03308, Charging Pump P-55C has Experienced a New Maintenance Rule Functional Failure, July 12, 2017 -
: CR-PLP-2017-03344, Found a Damaged #2 Suction Valve on P-55C, July 13, 2017
-
: CR-PLP-2017-03400, Operator Noticed a Large Puddle of Water on the Floor, July 17, 2017
-
: CR-PLP-2017-03416,
: EK-3015, Low Jacket Water Pressure was Illuminated on
: EG-30A, Diesel Generator 1-2 Annunciator Panel, July 18, 2017 -
: CR-PLP-2017-03555, P-55B Charging Pump Oil Pressure Reading Below the Acceptance Range, July 28, 2017 -
: CR-PLP-2017-03723,
: SV-0884B, Service Water to Emergency Diesel Gen K-6A, was Found De-Energized, August 8, 2017 -
: CR-PLP-2017-03986, Perform One-Time Tightness Checks for Power Cables Connected to Molded Case Switches Associate with P-55B, August 25, 2017 -
: CR-PLP-2017-04106, System Engineering has Identified a Potential Adverse Trend on the Emergency Diesel Generator System, September 5, 2017 
-
: CR-PLP-2017-04248, Priming Time During the Fuel Oil Transfer Tests on P-18A, Fuel Oil Transfer Pumps were Higher than Expected, September 14, 2017 -
: CR-PLP-2017-04294, Parameter Which Exceeds the Defined 'Alert' Level per the
: EPS-EDG System Monitoring Plan, September 19, 2017 -
: CR-PLP-2017-04354, P-55B Charging Pump Oil level was Higher than Expected and Foamy, September 22, 2017 -
: CR-PLP-2017-04378, P-55C, Charging Pump, has Oil in the Seal Lube Overflow Weir, September 25, 2017 -
: CR-PLP-2017-04498, P-55B, Charging Pump, Seal Lube Tank Line is Partially Clogged, October 3, 2017 -
: EC 38731, Guidance for Emergency Diesel Generator Gauge Panel Instrument Tubing Replacement, Revision 0 -
: EC 72289, Rotate Level Switch
: LS-1453 Diesel Generator 1-2 Control Level Switch, Revision 0 -
: EC 72298,
: LS-1453; Replacement of P-18A Fuel Oil Transfer Pump Level Switch, Revision 0 -
: EN-DC-205, Maintenance Rule Monitoring, Revision 6
-
: EN-DC-206, Maintenance Rule (a)(1) Process, Revision 3
-
: EN-DC-336, Plant Health Committee, Revision 11
-
: EN-QV-102, Quality Control Inspection Program, Revision 4 - Entergy Quality Assurance Program Manual, Revision 33 -
: EN-WM-105, Planning, Revision 19
- Justification for Excluding Planned Unavailability Associated with the 3
rd Quarter 2017
: LS-1453 Replacement and Piping Rework, July 19, 2017 - Maintenance Rule (a)(1) Action Plan Charging Pumps P-55A, P-55B, and P-55C, Revision 3
-
: MSPI-Emergency AC Power Performance Indicator Technique/Data Sheet, February 2017 - System Health Report, Emergency Diesel Generators, Q2, 2017 -
: VEN-M-12, Engine Control Diesel Generator 1-2 Schematic, Sheet 105(2), Revision 19
-
: VEN-M12, Schematic Diagram Engine Control Di esel Generator 1-1, Sheet 98(1), Revision 36 -
: VEN-M-12, Schematic Engine Control Diesel Generator 1-2, Sheet 105(1), Revision 31
-
: WO 421559, K-6B (Air Motor A) Starting Air Instruments -
: WO 424624, P-55B; 'B' Charging Pump, Replace/Adjust Packing -
: WO 444039, K-6B; Raw Water Tubing >G-30 Worn per
: EC 73831 Replace-VLC
-
: WO 454094, Test Spare Charging Pump Bladders in Stock
-
: WO 454097, P-55B; 'B' Charging Pump, Degraded Flow and Banging Noises
-
: WO 459272, Charging Pump, Shorten Pipe Between Block and First Elbow
-
: WO 471605, Broken Hanger JB24 - H3.14 -
: WO 472131, P-55A; 'A' Charging Pump, Tripped Upon Starting -
: WO 473397,
: LS-1453 Diesel Generator 1-2 Control Level Switch Will Not Stop P-18
-
: WO 478002,
: EMB-1105;, P-55C Motor, Check Connections and Retest
-
: WO 478628,
: LS-1453 (T-25B) Modify Piping to Raise LS on TK per
: EC-72289
-
: WO 478857, Charging Pump P-55C Tripped on Overcurrent Installed New Switches and Cables -
: WO 479465, K-6B; EDG 1-2 Broken Bolt Repair
-
: WO 479855,
: PS-1473;
: EK-0557 Alarm Unexpectedly - Check Calibration
-
: WO 481979,
: SV-0884B Failed to Energize When Engine was Secured
-
: WO 483390, P-55B; Check Tightness of Power Cables to Molded Case Switches on 'B' Charging Pump Breakers -
: WO 483391, P-55C; Check Tightness of Power Cables to Molded Case Switches on 'C' Charging Pump Breakers -
: WO 485338, P-55B; 'B' Charging Pump has Water in Oil
-
: WO 52505668, K-6B; 4 Cycle Au xiliary Systems Maintenance 
-
: WO 52734581, T-105A; 'A' Charging Pump Suction Accumulator Bladder Replacement -
: WO 52740494, T-105B; 'B' Charging Pump Suction Accumulator Bladder Replacement
-
: WO 52742966, 'C' Charging Pump Suction Accumulator Bladder Replacement -
: WT-WTPLP-2014-00325, Transfer Maintenance Rule (a)(1) Monitoring and Final (a)(1) Action Plan Process for Charging Pumps P-55A, P-55B, and P-55C to this Work Task, December 11, 2014 -
: WT-WTPLP-2017-00342, Transfer Maintenance Rule (a)(1) Monitoring and Final (a)(1) Action Plan Processing for the "Charging Pumps P-55A, P-55B, and P-55C" to this Work Task, August 29, 2017 1R13 Maintenance Risk Assessments and Emergent Work Control - Admin 4.02, Control of Equipment, Revision 77 -
: CR-PLP-2016-02173, Required Protected Train Postings Around P54C Containment Spray Pump were Instead Around P-67B, May 12, 2016 -
: CR-PLP-2017-00380, Weakness in Work Preparation, Scheduling and Execution Resulted in Placing the Plant in Unrecognized Risk, January 31, 2017 -
: CR-PLP-2017-02528, A Panel on the Back of C-12 Primary System Control, is Missing 3 of the 11 Screws Which Hold it On, July 26, 2017 -
: CR-PLP-2017-03031, Missed Opportunity to Appropriately Classify the Integrated Risk of
: WO 52664424-01, June 21, 2017 -
: CR-PLP-2017-03031, Missed Opportunity to Appropriately Classify the Integrated Risk of
: WO 52664424-01, June 21, 2017 -
: CR-PLP-2017-03529, During the Performance of
: RT-202B, Stop Work Criteria was Met, July 26, 2017 -
: CR-PLP-2017-03531, A Printed Sign Above Fire Station #7 Hose Reel is Partially Covered by a Cable Support Bracket, July 26, 2017 -
: CR-PLP-2017-03538, SPI Node Indications on the Plant Process Computer Were Lost, July 26, 2017 -
: CR-PLP-2017-03551, Troubleshooting Activities were Performed Without Having the Cover Page of
: EN-MA-125 Approved by a Supervisor and the Shift Manager, July 27, 2017 -
: CR-PLP-2017-03561, DOPS (Digital Outputs Processing System) Application was Generating Error Messages, July 28, 2017 -
: CR-PLP-2017-03563, Bad Pushbutton Switch on the Assembly is Causing a Loss of Communication Between the SPI Node and the Host Computers, July 28, 2017 -
: CR-PLP-2017-03565, During the Removal of the Fuel Oil from T-25B, 1-2 Diesel Fuel Oil Day Tank Approximately 2-3 Gallons Leaked Out onto the Floor, July 28, 2017 -
: CR-PLP-2017-03573, NRC Identified, EOOS was Incorrectly Updated During Completion of
: RT-202B, Control Room Heating, Ventilation and Air Conditioning Heat Removal Capability Testing, July 28, 2017 -
: CR-PLP-2017-03624, Door #116 was Found to be Unlatched, August 1, 2017 -
: CR-PLP-2017-03630, Broken Ground Connection to a 3/4 Inch Conduit in the Diesel Generator 1-2 Room, August 1, 2017 -
: CR-PLP-2017-03638, NRC Identified Compensatory Measure for Verifying No Severe Weather Forecasted was Not Logged Between 1540 and 1740 as Required, August 2, 2017 -
: CR-PLP-2017-03737, (NIOS) Identified Problem:
: The Work Order on
: SV-0884B was Not Statused as "Working", August 8, 2017 -
: CR-PLP-2017-03738, (NIOS) Identified:
: Foreign Material Exclusion (FME) Pre-Job Brief (PJB)/FME Plan Attachment 9.1 was Not Completed Prior to Work, August 8, 2017 
-
: CR-PLP-2017-03739, (NIOS) Identified Problem:
: Prerequisites were Placekept as Complete and Validated by the Supervisor Prior to All of the Actions Being Actually Completed, August 8, 2017 -
: CR-PLP-2017-03744, Door 170, the North Entrance to Both Diesel Generator Rooms from the Outside, Failed the Chalk Test Portion of its Yearly Inspection, August 9, 2017 -
: CR-PLP-2017-03757, Non-conforming Tag Placed on Old ESR Relays, August 9, 2017
-
: CR-PLP-2017-03758, Following Replacement of ESR Relays Observed a Contact Pressure Spring on ESR 2 had become Dislodged, August 9, 2017 -
: CR-PLP-2017-04066, There have been Three Occasions in which Operations has Logged the Compensatory Actions as Shiftly Instead of Hourly, August 31, 2017 -
: CR-PLP-2017-04259, Door Mechanism on Door-15 Equipment Room Missile Shield/Radiation, Malfunctioned while Trying to Exit, September 16, 2017 -
: CR-PLP-2017-04275, Adverse Condition was Discovered while Working on Door-15, September 18, 2017 -
: EC 62374, Risk Assessment for Blocking Open Door-170 - Outside Access to Both Emergency Diesel Generator 1-1 and Emergency Diesel Generator 1-2, Revision 0 -
: EC 62767, Risk Assessment for Blocking Open Door-141 (EDG 1-2 from Turbine Building Hallway) for Maintenance Activities, Revision 0 -
: EC 72836, Evaluation of Door-181 Open Time East Safeguards to Post Tension Tunnel, Revision 0 -
: EC 73469, Assessment of TGAPs in Door 170 Seal, Revision 0
-
: EN-FAP-WM-002, Critical Evolutions, Revision 4
-
: EN-MA-125, Troubleshooting Control of Maintenance Activities, Revision 20
-
: EN-OP-116, Infrequently Performed Tests or Evolutions, Revision 12
-
: EN-WM-104, On Line Risk Assessment, Revision 15 - Operations Log, Day Shift, Friday, July 28, 2017 - Operator's Risk Report, Friday, July 28, 2017
- Operator's Risk Report, Thursday, July 27, 2017
-
: PO-3, Alternate Incore and Excore Applications, Revision 10
-
: SOP-24, Ventilation and Air Conditioning System, Revision 75 -
: SOP-34, Palisades Plant Computer (PPC) System, Revision 36 -
: SWSO-4, Molluscicide Treatment of Service Water and Fire Protection Systems, Revision 22 - T-303, Emergency Diesel Generator 1-2 Overspeed Trip Setpoint Verification, Revision 16 -
: WO 478628,
: LS-1453 (T-25B) Modify Piping to Raise LS on TK per
: EC-72289 1R15 Operability Determinations and Functionality Assessments - Calculation No. 2007-03600, Post Loss of Cooling Accident Containment Sump pH Control Using Sodium Tetraborate (NaTB), Revision 0 -
: CR-PLP-2017-02456,
: RM-124 Sodium Tetraborate Basket Weights Reported is Less than the Required Minimum Weight, May 12, 2017 -
: CR-PLP-2017-02946, Nuclear Independent Oversight Identified Two Operability Determinations were Not Performed in Accordance with
: EN-OP-104, Operability Determination Process, June 14, 2017 -
: CR-PLP-2017-03722, During Performance of
: MO-7A-1, Operators Noted a Jacket Water Leak from 1-1 Emergency Diesel Generator Turbocharger Casing, August 8, 2017 -
: CR-PLP-2017-03723, After Completion of
: MO-7A-1, Emergency Diesel Generator 1-1 Testing,
: CV-0884, Diesel Generator 1-1 Service Water Inlet was Still in the Open Position, August 8, 2017 -
: CR-PLP-2017-03741, During Observation of the
: SOP-22 Start of K-6A, Emergency Diesel Generator 1-1, a Cloud of Exhaust Appeared, August 8, 2017 
- DBD 5.01, Diesel Engine and Auxiliary Systems, Revision 7 - DBD 5.03, Emergency Diesel Generator Performance Criteria, Revision 9
-
: RC-123, Sodium Tetraborate Decahydrate Buffering Tests, Revision 14 -
: RC-123, Sodium Tetraborate Decahydrate Buffering Tests, Revision 6 -
: RM-124, Sodium Tetraborate Basket Weights, Revision 3
-
: RM-124, Sodium Tetraborate Basket Weights, Revision 7
- Sodium Tetraborate Decahydrate Safety Data Sheet, March 26, 2012
-
: SOP-22, Emergency Diesel Generators, Revision 74
-
: VEN-M12, Schematic Diagram Engine Control Di esel Generator 1-1, Sheet 98(1), Revision 36 -
: WO 428910,
: RC-123, Sodium Tetraborate Decahydrate Buffering & Solubility -
: WO 429013,
: RM-124 Sodium Tetraborate Decahydrate Basket Weights 1R19 Post Maintenance Testing -
: ARP-7, DBA/NSD Sequencers, Attachment 2, Revision 101 -
: CR-PLP-2009-01237, Reactor Protection System Breaker 42-2 Failed to Trip, March 23, 2009
-
: CR-PLP-2016-03260, Received Alarm
: EK-1145, "Sequencer Trouble," Unexpectedly, July 18, 2016 -
: CR-PLP-2017-00837, During the Clutch Power Trip Circuit Test of the AD Matrix, Relay 3 had
a Slow Response Time, March 8, 2017 -
: CR-PLP-2017-02587, Reactor Protection System Breaker 42-2 Failed to Open when
: RPS-PB2, Reactor Trip Pushbutton at C-06, was Pressed, May 17, 2017 -
: CR-PLP-2017-02589, Y Phase Magnetic Pickup was Slightly Below Acceptance Criteria Value of 1600, May 17, 2017 -
: CR-PLP-2017-02590, Non-Conforming Part CR, May 18, 2017 -
: CR-PLP-2017-02593, Work Order Tasks Needed for Further Troubleshooting Support, May 18, 2017 -
: CR-PLP-2017-03659, Left Train Emergency Diesel Generator Load Sequencer Failure, August 3, 2017 -
: CR-PLP-2017-03671, Non-conformance Tracking CR for
: MC-34L101, 1-1 DG Load Sequencer, August 3, 2017 -
: CR-PLP-2017-03673, Programmable Processor Card was Found to be Defective and Could Not be Used, August 3, 2017 -
: CR-PLP-2017-04007, Sequencer (ESS-SEQ), has Exceeded Maintenance Rule Performance Criteria, August 28, 2017 -
: CR-PLP-2017-04273, At the Start of T-303, Jacket Water Leaks were Noted on the Following Cylinders; 2R, 7R, and 4L, September 18, 2017 -
: CR-PLP-2017-04278, Drager X-am Alarmed on NO2, September 18, 2017
-
: CR-PLP-2017-04280, DB Readings Taken in the Diesel Generator Room While the Diesel Generator was Running, September 18, 2017 -
: CR-PLP-2017-04282, Drager X-am Multi-Gas Monitor Alarmed on NO2, September 18, 2017 -
: CR-PLP-2017-04285, NIOS Identified:
: Emergency Diesel Generator (EDG) 1-2 Copper Instrument Air Line in Contact with Coated Steel Beams, September 19, 2017 -
: CR-PLP-2017-04314, Run Time Meter for K-1B (Gas Engine for C-3B, Diesel Generator Air Compressor), is Missing, September 20, 2017 -
: CR-PLP-2017-04336, Breaker 42-2/RPS, Reactor Protection System Control Rod Clutch Breaker was Not Shipped in a Timely Manner to a Vendor for a Failure Analysis, September 21, 2017 -
: CR-PLP-2017-04457, Found P-55B, 'B' Charging Pump, Seal Lube Tank Level at Approximately 45%, September 29, 2017 
-
: DBD-2.05, Reactor Protective System Safety Injection Signal Anticipated Transient Without SCRAM, Revision 7 -
: EN-OP-104, Operability Determination Process, Revision 11 -
: EOP-1.0, Standard Post-Trip Actions, Revision 19 - Forensic Inspection Report on Examination of GTE Relay for Palisades Nuclear Plant, September 14, 2017WO
: 485705, P-55B; 'B' Charging Pump, Shows Indication of Water Intrusion in Oil -
: GOP-8, Power Reduction and Plant Shutdown to Mode 2 or Mode 3
: 525°F, Revision 37 -
: MO-7A-2, Emergency Diesel Generator 1-2, Revision 95 - Operations Log, September 18, 2017 - Operations Log, Wednesday, May 17, 2017
- Operations Narrative Logs, August 3, 2017
-
: QI-3 Basis, Reactor Protection Matrix Logic Tests, Revision 0
-
: QI-3, Reactor Protection Matrix Logic Tests, Revision 7 -
: QO-1, Safety Injection System, Revision 69 -
: SOP-22, Emergency Diesel Generators, Revision 74
-
: SOP-2A, Chemical and Volume Control System, Revision 87
-
: SOP-36, Reactor Protective System and Anticipated Transient Without SCRAM (ATWS) System, Revision 13 -
: SOP-6, Reactor Control System, Revision 35 - T-303, Emergency Diesel Generator 1-2 Overspeed Trip Setpoint Verification, Revision 18
-
: VEN-M1-Q, Block Diagram Reactor Protective System, Sheet 114, Revision 13
-
: VEN-M1-Q, Reactor Protective System Schematic, Sheet 1198, Revision 76
-
: WO 453345, RPS/MR-AD3; Replace Relay Found Degraded per
: QI-3
-
: WO 475913, 42-2/ Reactor Protection System; Right Reactor Protection System Trip Breaker, did Not Open on Reactor Trip -
: WO 481586, Left Train Emergency Diesel Generator Load Sequencer Repair/Replace
-
: WO 485338, P-55B Charging Pump has Water in Oil
-
: WO 52646122, 42-1/RPS; Replace Breaker
-
: WO 52663788, T-303 - Diesel Generator 1-2 Emergency Diesel Generator Overspeed Trip Setpoint Test -
: WO 52759816,
: MO-7A-2, Emergency Diesel Generator 1-2 (K-6B) 1R22 Surveillance Testing - Admin 4.19, PCS Leak Rate Monitoring Program, Revision 6 -
: AOP-23, Primary Coolant Leak Basis, Revision 0 -
: AOP-23, Primary Coolant Leak, Revision 2
- COLR, Core Operating Limits Report, Revision 19
-
: CR-PLP-2016-04538, Core Exit Thermocouple (CET) #16 was Reading Erratically
-
: CR-PLP-2017-01570, Reactivity Anomaly per
: MT-10 is Greater than 0.3% Delta Rho, April 18, 2017 -
: CR-PLP-2017-02584, NIOS Identified: Adjustments to the Main Steam Bypass Valves were Performed Without a Procedure in Hand, May 17, 2017RT-191, Startup Physics Test Program,
: Revision 11 -
: CR-PLP-2017-02585, Several Instances Where (NCO) did Not Verbally Acknowledge the Reactor Engineer's Order, May 17, 2017 -
: CR-PLP-2017-02591,
: NI-5 Experienced a Noisy Signal to the Test Equipment -
: CR-PLP-2017-02616, Control Room Received
: EK-0601A Variable High Power Level Channel Trip,
: EK-0605A Variable High Power Level Channel Pre-Trip,
: EK-0917 Rod Withdrawal Prohibit, and
: EK-0606A High Power Rate Channel Pre-Trip / ASI for "D" Channel RPS, May 20, 2017 -
: CR-PLP-2017-02621, Quadrant Power Tilt Deviation Between Incores and Excores Exceeds 0.02 Acceptance Criteria, May 20, 2017 -
: CR-PLP-2017-02638, During Power Ascension, the Trends on Incore Detectors 16 (INCE-25R08), 17 (INCE-84B10), 24 (INCE-72G13), and 25 (INCE-71H13) Indicated that they were Not Fully Inserted, May 22, 2017 -
: CR-PLP-2017-02640, PIDAL Core Monitoring Software Output Cases were Not Available from the Uranium 2 Server, May 22, 1017 -
: CR-PLP-2017-02733, Determined that Primary Makeup (PMU) Water is Potentially Leaking Through
: CV-2155 Make-Up Stop, and
: CV-2165, Boric Acid Blender M-51 PMU Inlet Control
: Valves, May 31, 2017 -
: CR-PLP-2017-02755, Reciprocal Boron Worth (RBW) Measurement Difference of 17.7 ppm/%delta-rho does Not Meet the Review Criterion, June 1, 2017 -
: CR-PLP-2017-02783, Exceeded 2 of 3 Consecutive ULR>Baseline Mean +2 Standard Deviations, June 3, 2017 -
: CR-PLP-2017-02795, PCS Leak Rates Triggering Action Level 2 of Admin. 4.19, June 5, 2017
-
: CR-PLP-2017-02897, Containment Sump Rate of Rise is Currently 0.07 gpm, June 12, 2017
-
: CR-PLP-2017-02920, Packing of
: CV-2155 is Leaking Causing an Accumulation of Boric Acid Residue, June 13, 2017 -
: CR-PLP-2017-02928,
: MV-CVC2162, must be Opened by an NPO for Each Dilution, June 14, 2017 -
: CR-PLP-2017-03323, 120 Volt Electrical Outlet on the South Wall of the Cable Spreading Intermittently Working, July 12, 2017 -
: CR-PLP-2017-03583, PMT for
: WO 477426 Failed, July 30, 2017 -
: DWO-1, Operator's Daily/Weekly Items Modes 1, 2, 3, and 4, Revision 107 - M-202, Piping & Instrument Diagram Chemical & Volume Control System, Sheet 1A, Revision 64 - M-202, Piping & Instrument Diagram Chemical & Volume Control System, Sheet 1B, Revision 59 - M-202, Piping & Instrument Diagram Replacement Heat Tracing for CVC System, Sheet 3, Revision 16 - Model 1N, Connection Diagram, Model 1N Load Unit, October 5, 2004
- P-8A, 'A' Auxiliary Feedwater Pump IST Data, September 2016 through September 2017 - Palisades Cycle 26 Startup and Operations Report, April 2017
- PCS Leak Rate Monitoring Workbook, May 2017 - September 2017 - PCS Leakrate Snap Shot, June 6, 2017 -
: PNP-2016-059, Notification of Inoperability of One Core Exit Temperature Indication Channel, November 2, 2016 -
: QO-21, Inservice Test Procedure, Auxiliary Feedwater Pumps, Revision 49
-
: RE-135, Performance Test - Battery Charger Number 3 (ED-17), Revision 13 -
: SEP-CV-PLP-002, Check Valve Condition Monitoring and Inservice Testing Program, Revision 4 -
: SEP-ISI-PLP-002, ASME Code Boundaries for ASME Section XI Inservice Inspection Program, Revision 2 -
: SEP-PLP-IST-101, Inservice Testing of Plant Valves, Revision 4
-
: SEP-PLP-IST-102, Inservice Testing of Selected Safety-Related Pumps, Revision 3 -
: SOP-2A, Chemical and Volume & Control System, Revision 87 -
: SOP-6, Reactor Control System, Revision 35
-
: VEN-E-12A, System Block Diagram, Battery Capacity Test System 2000, Sheet 31, Revision 1 -
: WO 460289,
: MT-10 Core Monitoring 
-
: WO 460291,
: MT-10 Core Monitoring - Align with
: MT-10X1B (25% Power) -
: WO 460292,
: MT-10, Core Monitoring
-
: WO 475821,
: NI-5, LPPT Signal Noisy, Use
: NI-7 Contingency -
: WO 477425,
: CV-2155; Investigate if Leak By Exists in Valve and Adjust/Repair -
: WO 477426, Investigate if Leak By Exists in Valve and Adjust/Repair
-
: WO 52670066,
: RE-135-ED-17, Battery Charger Number 3 Performance Test
-
: WO 52678781,
: NI-5, I&C Support Work Order for LPPT
-
: WO 52680611,
: RT-101, Startup Physics Test Program -
: WO 52728173,
: MT-10, Core Monitoring 1EP2 Alert and Notification System Evaluation - 2015-2016 EP Public Information Booklet - 2017 EP Public Information Calendar - ANS Maintenance Records, July 2015 to June 2017 -
: CR-PLP-2015-04908, Failure of Sound on Siren #49, October 10, 2015 
-
: CR-PLP-2016-00813, Siren #14 Failed to Rotate and Sound, February 13, 2016
-
: CR-PLP-2016-01094, Siren #40 Communication Failure, March 3, 2016
- Documentation of PWS Monthly Tests, July 2015 to June 2017
- Federal Emergency Management Agency Letter, Provisions for Backup Alert and Notification (ANS) for the Palisades Nuclear Power Plant Emergency Planning Zone (EPZ), December 10, 2012 - Federal Emergency Management Agency Palisades Nuclear Plant Public ANS Approval Letter, December 20, 2002  - PAL PWS, Palisades Nuclear Plant Public Warning System Operating Procedure, Revision 22 - Palisade Nuclear Plant Public Warning System Replacement Project Design Report, October 2002 1EP3 Emergency Response Organization Staffing and Augmentation System -
: CR-PLP-2016-01860, Review for Possible Gaps in ERO Continuing Training, April 19, 2016 -
: CR-PLP-2017-02197, Emergency Preparedness (EP) Training for an Emergency Response Organization (ERO) Member Exceeded 90 days, May 5, 2017 - Current ERO Team Staffing, June 29, 2017
-
: EI-2.2, Emergency Staff Augmentation, Revision 17
- Emergency Response Organization Off-hours, Unannounced, Augmentation Response Test Records, July 2015 to June 2017  -
: EN-EP 310, Emergency Response Organization Notification System, Revision 5
-
: EN-TQ-110, Emergency Response Organization Training, Revision 12 - Palisades Nuclear Station On-Shift Staffing Analysis Final Report, Revision 3 1EP5 Maintenance of Emergency Preparedness - 2015 Palisades Radiological Medical Drill Report Summary, December 29, 2015 - 3rd Quarter 2015 Drill (Green Team) Emergency Planning Drill Report, September 10, 2015 - 4th Quarter 2015 Integrated Drill (Red Team) Emergency Planning Drill Report, January 6, 2016
- Andrews University Airpark Airport Authority Letter of Agreement, December 15, 2016 - April 13, 2016 Pre-NRC Exercise Emergency Planning Drill Report, May 9, 2016 - April 26, 2016 Pre-NRC Exercise Emergency Planning Drill Report, May 20, 2016
- Covert Fire Department Letter of Agreement, Dated 9, 2016
-
: CR-PLP-2015-06232,
: PIPP-02, Emergency Notification System, Revision 17, Contains Outdated Contact Information, December 9, 2015 
-
: CR-PLP-2016-00848, Control Room EP Job Aid
: GEN-012 is Not the Current Revision, February 16, 2016 -
: CR-PLP-2016-01084, Emergency Planning Job Aid
: GEN-007 Incorrect, March 3, 2016 -
: CR-PLP-2016-01499, Self-Assessment EP Program Negative Observation, March 28, 2016 -
: CR-PLP-2016-01928, Requirements for Completing Procedure Accuracy Reviews, April 25, 2016
-
: CR-PLP-2017-00536, Emergency Planning Drill Objective J.6 Evaluated as Needs Improvement, February 13, 2017 -
: CR-PLP-2017-01593, Palisades Emergency Planning Self-Assessment Negative Observation Noted, April 19, 2017 -
: EN-LI-102, Corrective Action Process, Revision 29 - Lakeland Regional Health System Letter of Agreement, August 9, 2016
-
: LO-PLPLO-2015-00084, Palisades Pre-NRC Exercise Assessment, February 26, 2016
: LO-PLPLO-2016-00057, Pre NRC Program In spection Assessment, April 17, 2017 - May 17, 2016 NRC Evaluated Emergency Planning Exercise Report, June 14, 2016 - Medic 1 Letter of Agreement, August 9, 2016  - Monthly Communications Test Records, July 2016 through June 2017
- Palisades Power Plant 2016 Population Update Analysis, September 21, 2016
-
: QA-7-2016-PLP-1, Quality Assurance Audit Report - Emergency Planning, May 19, 2016 
-
: QA-7-2017-PLP-1, Quality Assurance Audit Report - Emergency Planning, May 10, 2017 - Quarterly Emergency Communications Test Records, July 2016 through June 2017 - Semi-Annual Health Physics Drill 2016 Summary Report, September 6, 2016
- SEP Supplement 1, EAL Wall Chart, Revision 3
- SEP Supplement 2, Evacuation Time Estimate, Revision 0
- SEP, Palisades Nuclear Plant Site Emergency Plan, Revision 28
- South Haven Area Emergency Services Letter of Agreement, August 9, 2016  - South Haven Healthcare Systems Letter of Agreement, August 9, 2016 - WEBEX Blast Conference Line Test Records, July 2016 through June 2017
- West Michigan Airport Authority Letter of Agreement, September 15, 2016
-
: WS-RSD-T-001, Attachment 1, Emergency Preparedness Quarterly Test Check Sheets, July 2016 through June 2017
: 1EP6 Drill Evaluation - Emergency Planning Drill Scenario Package, August 16, 2017 - Palisades Site Emergency Plan Revision 28 - Palisades Site Emergency Plan Supplement 1, EAL Wall Charts, Revision 3 2RS1 Radiological Hazard Assessment and Exposure Controls -
: CR-PLP-2017-02160, Locked High Radiation Area Door Watch Left His Post, May 4, 2017
: 2RS5 Radiation Monitoring Instrumentation - 2017 Recalibration of the Canberra
: ABACOS-2000 Fastscan Counting System, January 5, 2017 -
: ASP-1 Certificate of Calibration, Various Dates
- Canberra iSolo Counter Certificate of Calibration, Various Dates -
: CR-PLP-2015-01372, RP Not Performing Annual Gamma Sensitive Portal Monitor Testing, April 2, 2015 -
: CR-PLP-2015-05578, Site RP Instrument Procedures As Left Acceptance Criteria, November 9, 2015 -
: CR-PLP-2016-03600, EAD Failed, August 3, 2016 
-
: EN-RP-303, Source Checking of Radiation Protection Instrumentation, Revision 4 -
: EN-RP-306, Calibration and Operation of the Eberline
: PM-1, Various Dates
-
: EN-RP-307, Operation and Calibration of the Eberline Personal Contamination Monitors, Various Dates -
: EN-RW-104 Attachment 9.1, 10 CFR Part 61 Waste Stream Sample Screening and Evaluation, June 13, 2017 - HP 9.93, Ludlum Model 54 Article Monitor, Revision 0
- Ludlum 177 Certificate of Calibration, Various Dates
- Ludlum M-2929 Certificate of Calibration, Various Dates - M-54 Calibration Data Sheet, Various Dates - Telepole Calibration Data Sheet, Various Dates
-
: TID 2016-05, Source Check Frequencies for Instruments Used for Contamination Monitoring at Radiological Control Area Exit Points, August 26, 2016 -
: WO 00429008 01,
: RI-86G-1, High Range Containment Monitor Calibration-Source Test -
: WO 52618168 01,
: RI-86G-2, High Range Containment Monitor Calibration-Online Portion -
: WO 52621590,
: RI-86B-9, Fuel Pool Area Monitor
: RIA-5709 Calibration -
: WO 52641428,
: RR-84C, Hi Range Noble Gas Effluent Monitor
: RIA-2327 Calibration
: 2RS6 Radioactive Gaseous and Liquid Effluent Treatment -
: COP-35, Ground Water Monitoring Program, Revision 5 -
: CR-PLP-2015-02963, REMP/RETS Basis Documents Do Not Include Sufficient Technical Justification, July 15, 2015 -
: CR-PLP-2015-03000, Technical Justification in
: RR-10-003 RETS Basis Document Not Consistent With ODCM, July 16, 2015 -
: CR-PLP-2016-01718, Radiological Air Sample Information From East Radwaste Facility, April 10, 2016 -
: CR-PLP-2016-04620, Tracking CR for Maintenance Rule Evaluations, September 28, 2016
-
: CR-PLP-2016-05350, During Performance of
: MR-14 the Check Source for
: RIA-1049 Failed Low Out of Tolerance, November 8, 2016 -
: CR-PLP-2016-05588, During Performance of WO#461029-01 Removed
: RE-1049 Detector and Replaced with New Detector, November 22, 2016 -
: CR-PLP-2017-00381, Instrument Parameters Not Adequately Implemented via
: DWR-10, January 31, 2017 -
: EN-CY-111, Radiological Groundwater Monitoring Program, Revision 7
-
: LO-PLPLO-2015-00082, Radiological Effluent Technical Specifications (RETS), February 24, 2017 - Palisades Nuclear Plant, Liquid Effluent Monitor Setpoint Calculations, February 28, 2014
- Release Order,
: LRW-052817
- Release Order,
: LRW-052917
- WGDT Release Authorization
: WG-032017, Waste Gas Decay Tank T-68A, April 13, 2017 - WGDT Release Authorization,
: WG-032017 - WGDT Release Authorization,
: WG-041217
-
: WO 00421566,
: RR-84D - Rad Gaseous Effluent Sample Flow Rate Calibration
-
: WO 00461029 01,
: RIA-1049 Check Source Failed Low Out of Tolerance
-
: WO 52578429,
: RR-9C - Turbine Building Sump Discharge Monitor RIA - 5211
-
: WO 52580636,
: RT-85C - SFP Ventilation HEPA & Charcoal Testing -
: WO 52585614 01,
: RR-9B - Radwaste Discharge Monitor
: RIA-1049 Calibration -
: WO 52683303 01,
: RR-9B - Radwaste Discharge Monitor
: RIA-1049 Calibration
-
: WO 52695730,
: RR-84A - RGEM
: RIA-2325 Calibration
-
: WO 52742286,
: DWR-10 - Stack Effluent Sampling Calculations 
-
: WO 52743560,
: DWR-10 - Stack Effluent Sampling Calculations 4OA1 Performance Indicator Verification -
: DWO-1, Operator's Daily/Weekly Items Modes 1, 2, 3, and 4, Revision 107 -
: EN-LI-114, Regulatory Performance Indicator Process, Revision 7
- NRC Performance Indicator Data, Emergency Preparedness - Alert and Notification System Reliability, 2
nd Quarter 2016 through 2
nd Quarter 2017 - NRC Performance Indicator Data, Emergency Preparedness - Drill/Exercise Performance,
: 2nd Quarter 2016 through 2
nd Quarter 2017 - NRC Performance Indicator Data, Emergency Preparedness - ERO Readiness,
: 2nd Quarter 2016 through 2
nd Quarter 2017 - NRC Performance Indicator Data, Mitigating Systems Performance Index - High Pressure Injection System, 3
rd Quarter 2016 through 2
nd Quarter 2017 - NRC Performance Indicator Data, Mitigating Systems Performance Index - Residual Heat Removal System, 3
rd Quarter 2016 through 2
nd Quarter 2017 - Operation's Daily Logs - Palisades MSPI Basis Document, July 12, 2017 4OA2 Problem Identification and Resolution -
: CR-PLP-2009-04394, Received Alarm
: EK-0560, Diesel Generator Day Tank T-25B High/Low Level Unexpectedly, September 21, 2009 -
: CR-PLP-2013-04545, At 1815 the Control Room Received Unexpected Alarm
: EK-0561, Diesel Generator Day Tank T-25B Hi-Lo Level, October 21, 2013 -
: CR-PLP-2015-02053, P-18A Should Not Have Started to Fill T-25, as Level was 90% and Stable When
: HS-1452 was Placed in Auto, May 18, 2015 -
: CR-PLP-2017-00233,
: EK-0650, Diesel Generator Day Tank T-25B Hi-Lo Level Alarm Unexpected, January 19, 2017 -
: CR-PLP-2017-00609, Received Alarm
: EK-0555, Diesel Generator Breaker 152-213 Trip Unexpectedly, February 20, 2017 -
: CR-PLP-2017-01285, Found that 2 Drawings did Not Show all the Jumpers that were Installed on 152-213CS, Diesel Generator 1-2 to Bus 1D Control Switch, March 31, 2017 -
: CR-PLP-2017-01286, Disposition the Old Circuit Breaker Control Switch 152-213CS which was Found Non-Conforming, March 31, 2017 -
: CR-PLP-2017-01290, While Performing Relay Calibrations for Breaker 152-213 (Diesel Generator 1-2 Breaker) Z-Phase Differential Relays' Induction Disk Contact Bent Backwards, March 31, 2017 -
: CR-PLP-2017-01291, While Performing
: MO-7A-2 Emergency Diesel Generator 1-2 Breaker
: 2-213 (Diesel Generator 1-2 to Bus 1D) Opened, and K-6B (Emergency Diesel Generator
: 1-2) Tripped, March 31, 2017 -
: CR-PLP-2017-01292, After Starting K-6B, Emergency Diesel Generator 1-2 the Red Running Light for K-6B was Flickering, March 31, 2017 -
: CR-PLP-2017-01642, P-18A, Fuel Oil Transfer Pump, would Not Stop Auto Filling T-25B, Emergency Diesel Generator 1-2 K-6B Day Tank, April 21, 2017 -
: CR-PLP-2017-02655, Failure of P-18A to Shutoff at the Desired Set Point, May 23, 2017
-
: CR-PLP-2017-02667, P-18A Fuel Oil Transfer Pump, did Not Start at the Normal Setpoint, May 24, 2017 -
: CR-PLP-2017-03007, Fuel Oil Transfer System Failed to Start the Fuel Oil Transfer Pump P-18A at the Start Setpoint of 83.75% in the Day Tank, T-25B, June 20, 2017 
-
: CR-PLP-2017-03427, During the Replacement of
: LS-1453 Diesel Generator 1-2 Control Level Switch, Editorial Errors were Identified on Level Setting Diagrams, July 19, 2017 -
: CR-PLP-2017-03576,
: LIA-1417 is Indicating with a 1-2 Percent Error, July 28, 2017 -
: DBD-5.01, Diesel Engine and Auxiliary Systems, Revision 7 - E-129, Schematic Diagram Stored Energy Operated Circuit Breaker 152-213, Sheet 6C, Revision 2 - E-139, Schematic Diagram Diesel Generator Breaker (152-213) sheet 1A, Revision 5
- E-14, Schematic Diagram Excitation, Meter and Relay Diesel Generators, Revision 23
- E-178, Schematic Diagram Diesel Oil Transfer Pumps, Sheet 1, Revision 22 - E-178, Schematic Diagram Diesel Oil Transfer Pumps, Sheet 4, Revision 4 -
: EC 69245,
: LS-1453; Change Switch Cover Configuration, Revision 0
-
: EC 72289, Rotate Level Switch
: LS-1453 Diesel Generator 1-2 Control Level Switch, Revision 0 -
: EC 72298,
: LS-1453, Replacement of P-18A Fuel Oil Transfer Pump Level Switch, Revision 0 -
: EN-WM-109, Scheduling, Revision 10 - M-214, Piping & Instrument Diagram Lube Oil, Fuel Oil & Diesel Generator Systems, Sheet 1, Revision 81 - M-398, Level Settings Diagram, Emergency Diesel Generator Day Tank T-25A & B, Sheet 38, Revision 6 - O2C-PAL-2017-0304, Station Response and Troubleshooting of
: LS-1453 (102 Emergency Diesel Generator Level Control) on May 23, 2017, May 24, 2017 -
: SOP-22, Emergency Diesel Generators, Revision 73
-
: SOP-22, Emergency Diesel Generators, Revision 74
-
: WI-SPS-E-08, Calibration of Bus 1C Protective Relays, Revision 5
-
: WI-SPS-E-09, Calibration of Bus 1D Protective Relays, Revision 7 -
: WI-SPS-E-18, Setup and Use of Manta
: MTS-5000 for Current Relays, Revision 3 -
: WO 00414304,
: LS-1452, Suspect T-25B Level Switch is Stuck Open
-
: WO 414304,
: LS-1452, Suspect T-25B Level Switch is Stuck Open
-
: WO 468698,
: SYN-0002, Perform Testing and Replacement of Synchroscope
-
: WO 468763, 152-213 EDG Output Breaker did Not Close -
: WO 471463, K-6B Fluctuating RPMs on Tachometer -
: WO 473397,
: LS-1453 Diesel Generator 1-2 Control Level Switch Will Not Stop P-18
-
: WO 478628,
: LS-1453 (T-25B) Modify Piping to Raise LS on Tank per
: EC-72289
-
: WO 52660491,
: PM-Bus 1D Relay Testing -
: WT-WTPLP-2016-00019, 2016 Engineering Routine Actions for Tracking, January 5, 2016 4AO3 Followup of Events and Notices of Enforcement Discretion -
: CR-PLP-2017-02601, RPS Actuation Earlier that Anticipated, May 19, 2017 - E-120, Schematic Diagram, Turbine Generator Protection - Coast Down, Revision 22
- E-121, Schematic Diagram, Turbine Control, Sheet 1A, Revision 8 - E-121, Schematic Diagram, Turbine Control, Sheet 2, Revision 31 - E-17, Logic Diagram, Turbine-Generator Trips and Fast Transfer, Sheet 9, Revision 25
-
: EN-LI-121-01, Trend Codes, Revision 9
- Night and Standing Order Log, August 3, 2017
-
: PO-1, Operations Pre-Startup Tests, Revision 17
-
: VEN-M201, Terminal Block Wiring Diagram, Section C04-2, Sheet 66, Revision 68 -
: VEN-MI-Q, Input Signal Connections to Auxiliary Trip Units Schematics, Sheet 1038, Revision 6
==LIST OF ACRONYMS==
: [[USED]] [[]]
: [[AC]] [[Alternating Current]]
: [[ACA]] [[Adverse Condition Analyses]]
: [[ACE]] [[Apparent Cause Evaluation]]
: [[ADAMS]] [[Agencywide Documents Access and Management System]]
: [[ANS]] [[Alert and Notification System]]
: [[CAP]] [[Corrective Action Program]]
: [[CFR]] [[Code of Federal Regulations]]
: [[CR]] [[Condition Report]]
: [[DEP]] [[Drill/Exercise Performance]]
: [[DG]] [[Diesel Generator]]
: [[EP]] [[Emergency Preparedness]]
: [[ERO]] [[Emergency Response Organization]]
: [[HRA]] [[High Radiation Area]]
: [[IMC]] [[Inspection Manual Chapter]]
: [[IP]] [[Inspection Procedure]]
: [[IR]] [[Inspection Report]]
: [[LER]] [[Licensee Event Report]]
: [[MSPI]] [[Mitigating Systems Performance Index]]
: [[NCV]] [[Non-Cited Violation]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NRC]] [[]]
: [[U.S.]] [[Nuclear Regulatory Commission]]
: [[ODCM]] [[Offsite Dose Calculation Manual]]
: [[PI]] [[Performance Indicator]]
: [[RCS]] [[Reactor Cooling System]]
: [[RPS]] [[Reactor Protection System]]
: [[SSC]] [[Structures, Systems, and Components]]
: [[TS]] [[Technical Specification]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
: [[URI]] [[Unresolved Item]]
: [[WO]] [[Work Order]]
}}
}}

Latest revision as of 09:18, 19 December 2019

NRC Integrated Inspection Report 05000255/2017003
ML17299A146
Person / Time
Site: Palisades Entergy icon.png
Issue date: 10/25/2017
From: Eric Duncan
Region 3 Branch 3
To: Arnone C
Entergy Nuclear Operations
References
IR 2017003
Download: ML17299A146 (65)


Text

UNITED STATES October 25, 2017

SUBJECT:

PALISADES NUCLEAR PLANTNRC INTEGRATED INSPECTION REPORT 05000255/2017003

Dear Mr. Arnone:

On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Palisades Nuclear Plant. On October 18, 2017, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The enclosed report represents the results of this inspection.

Based on the results of this inspection, the NRC has identified one issue that was evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has also determined that a violation is associated with this issue. Because condition reports were initiated to address this issue, this violation is being treated as a Non-Cited Violation (NCV), consistent with Section 2.3.2 of the NRC Enforcement Policy. This NCV is described in the subject inspection report. Further, the inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.

If you contest the violation or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Palisades Nuclear Plant.

In addition, if you disagree with the cross-cutting aspect assignment to the finding discussed in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Palisades Nuclear Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Eric Duncan, Chief Branch 3 Division of Reactor Projects Docket No. 50-255 License No. DPR-20 Enclosure:

Inspection Report 05000255/2017003 cc: Distribution via LISTSERV

SUMMARY

Inspection Report 05000255/2017003, 07/01/2017 - 09/30/2017; Palisades Nuclear Plant;

Problem Identification & Resolution.

This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. One Green finding was identified by the inspectors.

The finding involved a Non-Cited Violation (NCV) of U.S. Nuclear Regulatory Commission (NRC) requirements. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," dated April 29, 2015.

Cross-cutting aspects are determined using IMC 0310, "Aspects Within the Cross-Cutting Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision

NRC Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance and an associated NCV of Technical Specification (TS) 5.4.1, Procedures, was self-revealed on March 31, 2017, when the 1-2 Diesel Generator (DG) tripped during performance of monthly TS surveillance procedure MO-7A-2, Emergency Diesel Generator 1-2. Specifically, during conduct of the monthly surveillance procedure, restoration activities associated with maintenance of breaker 152-213, 1-2 DG to Bus 1D, were being performed. When maintenance personnel closed the trip cutouts for the Z-phase of the 1-2 DG differential overcurrent relay, an unbalanced current flow into the differential relay resulted in relay actuation.

This actuation resulted in a trip of the output breaker and subsequently the 1-2 DG. The trip caused a delay in the TS surveillance activities and resulted in the extended unavailability and inoperability of the 1-2 DG. The licensee entered this issue into their corrective action program (CAP) as condition report (CR) CR-PLP-2017-01291.

Corrective actions included retesting the 1-2 DG and updating the work instructions associated with the differential overcurrent relays to include caution statements that opening or closing trip cutouts for the relays while the output breakers from the DGs to the associated buses were closed could cause the differential relays to actuate and trip the DG.

The issue was determined to be more than minor in accordance with IMC 0612,

Appendix B, Issue Screening, because it was associated with the Mitigating Systems cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding screened as having very low safety significance (Green) in accordance with IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, since the inspectors answered No to all screening questions. The finding had a cross-cutting aspect in the area of Human Performance, in the Work Management aspect, for the licensees failure to identify and manage risk commensurate to the work (H.5). (Section 4OA2)

Licensee-Identified Violations

A violation of very low safety significance or Severity Level IV that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's CAP. This violation and corrective action tracking number is listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period operating at full power. The unit operated at or near full power for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Readiness for Impending Adverse Weather ConditionGeo-Magnetic Storm Forecast

a. Inspection Scope

A geo-magnetic storm disturbance with a K-index greater than or equal to seven with the potential to influence the plant was forecast on September 7, 2017. The inspectors reviewed the licensees preparations for the impending weather conditions and conducted independent walkdowns of the plants alternating current (AC) power systems. The inspectors verified that plant procedures for the reliability and continued availability of the offsite and onsite power systems were appropriate. The inspectors also reviewed the licensees communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged in a timely manner when issues arose to take any necessary actions. The inspectors reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • B high pressure safety injection train;
  • alternate chemical and volume control system dilution pathway.

The inspectors selected these systems based on their risk significance relative to the Reactor Safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, the Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.

The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.

The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on the availability, accessibility, and condition of firefighting equipment in the following risk-significant plant areas:

  • Fire Areas 6 & 8: diesel generator (DG) 1-2 and fuel oil day tank rooms, elevation 590;
  • Fire Areas 5 & 7: DG 1-1 and fuel oil day tank rooms, elevation 590;
  • Fire Area 26: southwest cable penetration room, elevations 590 and 607;
  • Fire Area 3: 1D switchgear room and north cableway, elevations 607 and 625';

and

  • Fire Area 9: screenhouse, elevation 590.

The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.

b. Findings

No findings were identified.

.2 Annual Fire Protection Drill Observation

a. Inspection Scope

On September 15, September 20, and September 27, 2017, the inspectors observed fire brigade activation drills for a fire in bus 1B. Based on these observations, the inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee staff identified deficiencies, openly discussed them in a self-critical manner at the drill debrief, and took appropriate corrective actions. Specific attributes evaluated were:

  • proper wearing of turnout gear and self-contained breathing apparatus;
  • proper use and layout of fire hoses;
  • employment of appropriate firefighting techniques;
  • sufficient firefighting equipment brought to the scene;
  • effectiveness of fire brigade leader communications, command, and control;
  • search for victims and propagation of the fire into other plant areas;
  • smoke removal operations;
  • utilization of pre-planned strategies;
  • adherence to the pre-planned drill scenario; and
  • drill objectives.

Documents reviewed are listed in the Attachment to this report.

These activities constituted one annual fire protection inspection sample as defined in IP 71111.05-05.

b. Findings

No findings were identified.

1R06 Flooding

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk-important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors reviewed flood analyses and design documents, including the UFSAR, engineering calculations, and abnormal operating procedures to identify licensee commitments. The inspectors also reviewed the licensees corrective action documents with respect to past flood-related items identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following plant areas to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and were operable, and that the licensee complied with its commitments:

Documents reviewed during this inspection are listed in the Attachment to this report.

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

Because the licensee reported finding several hundred gallons of water, some of which covered cables in Manhole 4, the inspectors elected to also perform an underground cable vaults inspection sample. This inspection sample is documented in Section 1R06.2.

b. Findings

No findings were identified.

.2 Underground Vaults

a. Inspection Scope

The inspectors selected underground bunkers/manholes subject to flooding that contained cables whose failure could disable risk-significant equipment. The inspectors determined whether the cables were submerged, whether splices were intact, and whether appropriate cable support structures were in place. In those areas where dewatering devices were used, such as a sump pump, the inspectors determined whether the device was operable and level alarm circuits were set appropriately to ensure that the cables would not be submerged. In those areas without dewatering devices, the inspectors verified that drainage of the area was available, or that the cables were qualified for submerged conditions. The inspectors also reviewed the licensees corrective action documents with respect to past submerged cable issues identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following underground bunkers/manholes subject to flooding:

  • Manholes 1, 2, 3, and 4.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one underground vaults sample as defined in IP 71111.06-05.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification

a. Inspection Scope

On August 22, 2017, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification training. The inspectors verified that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and that training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal, alarm response, and emergency operating procedures;
  • timely control board operation and manipulations;
  • oversight and direction from supervisors;
  • group dynamics involved in crew performance; and
  • ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program simulator sample as defined in IP 71111.11-05.

b. Findings

No findings were identified.

.2 Annual Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of the Annual Operating Test administered by the licensee from February 27, 2017 through March 30, 2017, required by Title 10 of the Code of Federal Regulations (CFR) 55.59(a). The results were compared to the thresholds established in Inspection Manual Chapter (IMC) 0609, Appendix I, Licensed Operator Requalification Significance Determination Process, to assess the overall adequacy of the licensees licensed operator requalification training program to meet the requirements of 10 CFR 55.59. (02.02)

This inspection constituted one annual licensed operator requalification examination results sample as defined in Inspection Procedure 71111.11-05.

a. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk-significant systems:

  • emergency DGs; and
  • charging system.

The inspectors reviewed events including those in which ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

The inspector performed a quality review for the DGs, as discussed in IP 71111.12, Section 02.02.

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly maintenance effectiveness sample and one quality control sample as defined in IP 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • Emergent work on the control rod secondary position indication system concurrent with LS-1453, 1-2 DG fuel oil day tank level switch, modification;
  • emergent troubleshooting and repairs to ESR1 & ESR2, 1-1 DG engine start relays; and
  • increased plant risk for planned 1-2 DG overspeed trip test, diving activities, and emergent door 15 (part of the control room heating, ventilation and air conditioning boundary) repairs.

These activities were selected based on their potential risk significance relative to the Reactor Safety cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

Documents reviewed during this inspection are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted three samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functional Assessments

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • operability of containment sodium tetraborate baskets after not meeting the acceptance criteria of the surveillance test; and
  • immediate operability of 1-1 DG after failure of CV-0884B, 1-1 DG service water inlet valve, to close.

The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.

This operability inspection constituted two samples as defined in IP 71111.15-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance testing activities to verify that procedures and testing activities were adequate to ensure system operability and functional capability:

  • left channel load sequencer surveillance testing after replacement;
  • functional testing of RPS breaker after replacement; and
  • test start of B charging pump after troubleshooting and emergent maintenance of baffle packing and adjusters.

These activities were selected based upon the SSCs ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted five post-maintenance testing samples as defined in IP 71111.19-05.

b. (Open) Unresolved Item: Left Train Emergency Diesel Generator Load Sequencer Failure

Introduction:

The inspectors identified an Unresolved Item (URI) associated with the failure of the left train emergency DG load sequencer to run its program. Since this sequencer is required for left train DG operability, this condition resulted in an unanticipated entry into a TS shutdown action statement. The cause of this failure is currently unknown, pending the results of a vendor evaluation of a failed load sequencer component.

Description:

On August 3, 2017, the control room received alarm EK-1145, Sequencer Trouble, unexpectedly. The operators identified that the indication lights were not lit on the left channel load sequencer, MC-34L101; declared the associated DG inoperable; and entered the appropriate TS action statement. The failed sequencer was removed and replaced with a new module that was satisfactorily post-maintenance tested and the left train EDG was subsequently declared operable on August 4, 2017.

The failed sequencer was sent to an on-site lab for further troubleshooting. No obvious visual signs of failure were identified and the electrolytic capacitors in the module all tested satisfactorily. The module was then bench tested using a test program, which identified that although it would power up, no program would run. The licensee completed an equipment failure evaluation to review the bench test data, along with information collected in the failure modes analysis, and determined that the direct cause of the failure was a memory fault within the sequencer module that caused the sequencer to lock-up and not run its program. A fault in the memory module, memory processing interface circuitry, or the executive module could have caused the sequencer to lock up. At the end of the inspection period, further examination by the vendor was required and in progress to determine the exact initiating point of the fault.

In addition to replacing the failed sequencer, the licensees immediate corrective actions included inspecting the right train load sequencer and completing the quarterly surveillance test to ensure proper operation; the results of which were satisfactory. A plant operating experience review was conducted and did not identify any prior memory failures on the load sequencers. Once the vendors evaluation is complete, the licensee plans to re-assess the failure mechanism and any additional corrective actions required.

This item is considered unresolved, pending the inspectors review of the vendor analysis and any changes made to the equipment failure evaluation, to determine if this issue constitutes a performance deficiency and/or violation of NRC requirements.

(URI 05000255/2017003-01, Left Train Emergency Diesel Generator Load Sequencer Failure)c. (Open) Unresolved Item: Failure Mechanism of 42-2/RPS Reactor Protection System Breaker Failure to Open

Introduction:

The inspectors identified an URI associated with the failure mechanism of the 42-2/RPS control rod clutch breaker failure to open. Specifically, at the end of the inspection period the licensee was working to understand the cause of the breaker failure and determine the actions required to address the failure mechanism.

Description:

On May 17, 2017, the licensee conducted a shutdown to complete emergent repairs to a leaking seal identified on control rod drive mechanism 40. In accordance with GOP-8, Power Reduction and Plant Shutdown to Mode 2 or Mode 3 525°F, the operators depressed the reactor trip pushbutton from the EC-06, reactor protection system panel. When the pushbutton was depressed, the reactor did not trip as expected. The operators successfully tripped the reactor using the reactor trip pushbutton on the EC-02, primary process and reactor controls console. The licensee identified that the 42-1/RPS breaker tripped as expected when the reactor trip pushbutton on the EC-06 panel was depressed, however, the 42-2/RPS breaker did not trip as expected. This resulted in the reactor trip not occurring as expected when the reactor trip pushbutton on the EC-06 panel was depressed as both breakers are required to open to result in a reactor trip.

The licensee performed troubleshooting activities to determine the cause of the 42-2/RPS breaker failure. The direct cause of the breaker failure was found to be the 42-2/RPS breaker undervoltage release mechanism failing to provide enough downward force to fully depress the trip plunger. This resulted in a physical failure of the breaker to open. At the end of the inspection period, the cause of this physical failure mode was unknown. The licensees equipment failure evaluation identified that it could be age-related degradation or a physical degradation of the breaker. As a corrective action, a failure analysis of the breaker was planned. Once the failure analysis is complete, the licensee plans to re-assess the failure mechanism and determine any additional corrective actions that are required to address the issue. This item is considered unresolved, pending the inspectors review of the failure analysis and any changes made to the equipment failure evaluation, to determine if this issue constitutes a performance deficiency and/or violation of NRC requirements. (URI 05000255/2017003-02, Cause of 42-2/Reactor Protection System Breaker Failure to Open)

1R22 Surveillance Testing

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • RE-135, battery charger No. 3 performance test (routine);
  • RT-191, low power physics testing (routine);

The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  • were acceptance criteria clearly stated, sufficient to demonstrate operational readiness, and consistent with the system design basis;
  • was plant equipment calibration correct, accurate, and properly documented;
  • were as-left setpoints within required ranges; and was the calibration frequency in accordance with TSs, the UFSAR, plant procedures, and applicable commitments;
  • was measuring and test equipment calibration current;
  • was the test equipment used within the required range and accuracy, and were applicable prerequisites described in the test procedures satisfied;
  • did test frequencies meet TS requirements to demonstrate operability and reliability;
  • were tests performed in accordance with the test procedures and other applicable procedures;
  • were jumpers and lifted leads controlled and restored where used;
  • were test data and results accurate, complete, within limits, and valid;
  • was test equipment removed following testing;
  • where applicable for IST activities, was testing performed in accordance with the applicable version of Section XI of the ASME Code and were reference values consistent with the system design basis;
  • was the unavailability of the tested equipment appropriately considered in the performance indicator (PI) data;
  • were test results not meeting acceptance criteria addressed with an adequate operability evaluation or was the system or component declared inoperable;
  • was the reference setting data accurately incorporated into the test procedure;
  • was equipment returned to a position or status required to support the performance of its safety functions following testing;
  • were problems identified during the testing appropriately documented and dispositioned in the licensees CAP;
  • were annunciators and other alarms demonstrated to be functional and were setpoints consistent with design requirements; and
  • were alarm response procedure entry points and actions consistent with the plant design and licensing documents.

This inspection constituted two routine surveillance testing samples, one in-service test sample, and one reactor coolant system leak detection inspection sample, as defined in IP 71111.22, Sections-02 and-05.

b. Findings

No findings were identified.

1EP2 Alert and Notification System Evaluation

.1 Alert and Notification System Evaluation

a. Inspection Scope

The inspectors reviewed documents, and conducted discussions with Emergency Preparedness (EP) staff and management regarding the operation, maintenance, and periodic testing of the back-up and primary Alert and Notification System (ANS) in Palisade Nuclear Plants plume pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and the daily and monthly operability records from July 2015 through July 2017. Information gathered during document reviews and interviews was used to determine whether the ANS equipment was maintained and tested in accordance with Emergency Plan commitments and procedures. Documents reviewed are listed in the Attachment to this report.

This ANS inspection constituted one sample as defined in IP 71114.02

b. Findings

No findings were identified.

1EP3 Emergency Response Organization Staffing and Augmentation System

.1 Emergency Response Organization Staffing and Augmentation System

a. Inspection Scope

The inspectors reviewed and discussed with plant EP management and staff the emergency plan commitments and procedures that addressed the primary and alternate methods of initiating an Emergency Response Organization (ERO) activation to augment the on-shift staff as well as the provisions for maintaining the plants ERO team and qualification lists. The inspectors reviewed reports and a sample of CAP records of unannounced off-hour augmentation drills and call-in tests, which were conducted from July 2015 through July 2017, to determine the adequacy of the drill critiques and associated corrective actions. The inspectors also reviewed a sample of the training records of approximately 15 ERO personnel who were assigned to key and support positions, to determine the status of their training as it related to their assigned ERO positions. Documents reviewed are listed in the Attachment to this report.

This ERO augmentation testing inspection constituted one sample as defined in IP 71114.03.

b. Findings

No findings were identified.

1EP5 Maintenance of Emergency Preparedness

.1 Maintenance of Emergency Preparedness

a. Inspection Scope

The inspectors reviewed a sample of nuclear oversight staff audits of the EP Program to determine whether these independent assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and samples of CAP records associated with the 2016 biennial exercise, as well as various EP drills conducted in 2015, 2016 and 2017 to determine whether the licensee fulfilled drill commitments and to evaluate the licensees efforts to identify, track, and resolve issues identified during these activities. The inspectors reviewed a sample of EP items and corrective actions related to the licensee's EP Program and activities to determine whether corrective actions were completed in accordance with the sites CAP.

Documents reviewed are listed in the Attachment to this report.

This correction of EP weaknesses and deficiencies inspection constituted one sample as defined in IP 71114.05.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee EP drill on August 16, 2017, to identify any weaknesses or deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the control room simulator, technical support center, and operations support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the CAP. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in IP 71114.06-06.

b. Findings

No findings were identified.

RADIATION SAFETY

2RS1 Radiological Hazard Assessment and Exposure Controls

.1 High Radiation Area and Very High Radiation Area Controls (02.06)

a. Inspection Scope

The inspectors assessed the controls for high radiation areas (HRAs) greater than 1 rem/hour and areas with the potential to become high radiation areas greater than 1 rem/hour for compliance with TSs and procedures.

These inspection activities supplemented those documented in IR 05000255/2017002 and constituted a complete sample as defined in IP 71124.01-05.

b. Findings

No findings were identified.

2RS5 Radiation Monitoring Instrumentation

.1 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors assessed select portable survey instruments that were available for use for current calibration and source check stickers, and instrument material condition and operability.

The inspectors observed licensee staff demonstrate performance checks of various types of portable survey instruments. The inspectors assessed whether high-range instruments responded to radiation on all appropriate scales.

The inspectors walked down area radiation monitors and continuous air monitors to determine whether they were appropriately positioned relative to the radiation sources or areas they were intended to monitor. The inspectors compared monitor response with actual area conditions for selected monitors.

The inspectors assessed the functional checks for select personnel contamination monitors, portal monitors, and small article monitors to verify they were performed in accordance with the manufacturers recommendations and licensee procedures.

These inspection activities constituted one complete sample as defined in IP 71124.05-05.

b. Findings

No findings were identified.

.2 Calibration and Testing Program (02.03)

a. Inspection Scope

The inspectors assessed laboratory analytical instruments used for radiological analyses to determine whether daily performance checks and calibration data indicated that the frequency of the calibrations was adequate and there were no indications of degraded instrument performance. The inspectors assessed whether appropriate corrective actions were implemented in response to indications of degraded instrument performance.

The inspectors reviewed the methods and sources used to perform whole body count functional checks before daily use and assessed whether check sources were appropriate and aligned with the plants isotopic mix. The inspectors reviewed whole body count calibration records since the last inspection and evaluated whether calibration sources were representative of the plant source term and that appropriate calibration phantoms were used. The inspectors looked for anomalous results or other indications of instrument performance problems.

The inspectors reviewed select containment high-range monitor calibration and assessed whether an electronic calibration was completed for all range decades, with at least one decade at or below 10 rem/hour calibrated using an appropriate radiation source, and calibration acceptance criteria was reasonable.

The inspectors reviewed select monitors used to survey personnel and equipment for unrestricted release to assess whether the alarm setpoints were reasonable under the circumstances to ensure that licensed material was not released from the site. The inspectors reviewed the calibration documentation for each instrument selected and discussed the calibration methods with the licensee to determine consistency with the manufacturers recommendations.

The inspectors reviewed calibration documentation for select portable survey instruments, area radiation monitors, and air samplers. The inspectors reviewed detector measurement geometry and calibration methods for portable survey instruments and area radiation monitors calibrated onsite and observed the licensee demonstrate use of the instrument calibrator. The inspectors assessed whether appropriate corrective actions were taken for instruments that failed performance checks or were found significantly out of calibration, and whether the licensee had evaluated the possible consequences of instrument use since the last successful calibration or performance check.

The inspectors reviewed the current output values for instrument calibrators. The inspectors assessed whether the licensee periodically measured calibrator output over the range of the instruments used with measuring devices that had been calibrated by a facility using National Institute of Standards and Technology traceable sources and whether corrective factors for these measuring devices were properly applied in its output verification.

The inspectors reviewed the licensees 10 CFR Part 61, Licensing Requirements for Land Disposal of Radioactive Waste, source term to assess whether calibration sources used were representative of the types and energies of radiation encountered in the plant.

These inspection activities constituted one complete sample as defined in IP 71124.05-05.

b. Findings

No findings were identified.

.3 Problem Identification and Resolution (02.04)

a. Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring instrumentation were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involved radiation monitoring instrumentation.

These inspection activities constituted one complete sample as defined in IP 71124.05-05.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

.1 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors walked down select effluent radiation monitoring systems to evaluate whether the monitor configurations aligned with Offsite Dose Calculation Manual (ODCM) descriptions and to observe the material condition of the systems.

The inspectors walked down selected components of the gaseous and liquid discharge systems to evaluate whether equipment configuration and flow paths aligned with plant documentation and to assess equipment material condition. The inspectors also assessed whether there were potential unmonitored release points, building alterations which could impact effluent controls, and ventilation system leakage that communicated directly with the environment.

For equipment or areas associated with the systems selected for review that were not readily accessible, the inspectors reviewed the licensee's material condition surveillance records.

The inspectors walked down filtered ventilation systems to assess for conditions such as degraded high efficiency particulate air/charcoal banks, improper alignment, or system installation issues that would impact the performance or the effluent monitoring capability of the effluent system.

As available, the inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluents to evaluate whether appropriate treatment equipment was used and the processing activities aligned with discharge permits.

The inspectors determined if the licensee had made significant changes to their effluent release points.

As available, the inspectors observed selected portions of the routine processing and discharging of liquid waste to determine if appropriate effluent treatment equipment was being used, and whether radioactive liquid waste was being processed and discharged in accordance with procedure requirements and aligned with discharge permits.

These inspection activities constituted one complete sample as defined in IP 71124.06-05.

b. Findings

No findings were identified.

.2 Calibration and Testing Program (02.03)

a. Inspection Scope

The inspectors reviewed calibration and functional tests for select effluent monitors to evaluate whether they were performed consistent with the ODCM. The inspectors assessed whether National Institute of Standards and Technology traceable sources were used, primary calibration represented the plant nuclide mix, secondary calibrations verified the primary calibration, and calibration encompassed the alarm setpoints.

The inspectors assessed whether effluent monitor alarm setpoints were established as provided in the ODCM and procedures.

The inspectors evaluated the basis for changes to effluent monitor alarm setpoints.

These inspection activities constituted one complete sample as defined in IP 71124.06-05.

b. Findings

No findings were identified.

.3 Sampling and Analyses (02.04)

a. Inspection Scope

The inspectors reviewed select effluent sampling activities and assessed whether adequate controls had been implemented to ensure representative samples were obtained.

The inspectors reviewed select effluent discharges made with inoperable effluent radiation monitors and assessed whether controls were in place to ensure compensatory sampling was performed consistent with the ODCM and that those controls were adequate to prevent the release of unmonitored effluents.

The inspectors determined whether the facility was routinely relying on the use of compensatory sampling in lieu of adequate system maintenance.

The inspectors reviewed the results of the inter-laboratory comparison program to evaluate the quality of the radioactive effluent sample analyses and assessed whether the inter-laboratory comparison program included hard-to-detect isotopes as appropriate.

These inspection activities constituted one complete sample as defined in IP 71124.06-05.

b. Findings

No findings were identified.

.4 Instrumentation and Equipment (02.05)

a. Inspection Scope

The inspectors reviewed the methodology used to determine the effluent stack and vent flow rates to determine if the flow rates were consistent with plant documentation, and whether differences between assumed and actual stack and vent flow rates affected the results of the projected public dose.

The inspectors assessed whether surveillance test results for TS required ventilation effluent discharge systems met TS acceptance criteria.

The inspectors assessed calibration and availability for select effluent monitors used for triggering emergency action levels or for determining protective action recommendations.

These inspection activities constituted one complete sample as defined in IP 71124.06-05.

b. Findings

No findings were identified.

.5 Dose Calculations (02.06)

a. Inspection Scope

The inspectors reviewed significant changes in reported dose values compared to the previous radiological effluent release report to evaluate the factors which may have resulted in the change.

The inspectors reviewed radioactive liquid and gaseous waste discharge permits to assess whether the projected dose to members of the public were accurate.

The inspectors evaluated the isotopes included in the source term to assess whether analysis methods were sufficient to satisfy detectability standards. The review included the current Part 61 analyses to ensure hard-to-detect radionuclides were included in the source term.

The inspectors reviewed changes in the licensees offsite dose calculations and evaluated whether those changes were consistent with the ODCM and Regulatory Guide 1.109. The inspectors reviewed meteorological dispersion and deposition factors used in the ODCM and effluent dose calculations and determined whether appropriate factors were being used for public dose calculations.

The inspectors reviewed the latest Land Use Census to assess whether changes had been factored into the dose calculations.

For select radioactive waste discharges, the inspectors evaluated whether the calculated doses were within the 10 CFR, Part 50, Appendix I and TS dose criteria.

The inspectors reviewed select records of abnormal radioactive waste discharges to ensure the discharges were monitored by the discharge point effluent monitor.

Discharges made with inoperable effluent radiation monitors, or unmonitored leakages were reviewed to ensure that an evaluation was made to account for the source term and projected dose to the public.

These inspection activities constituted one complete sample as defined in IP 71124.06-05.

b. Findings

No findings were identified.

.6 Problem Identification and Resolution (02.07)

a. Inspection Scope

The inspectors assessed whether problems associated with the effluent monitoring and control program were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. In addition, the inspectors evaluated the appropriateness of the corrective actions for a selected sample of problems documented by the licensee involving radiation monitoring and exposure controls.

These inspection activities constituted one complete sample as defined in IP 71124.06-05.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Drill/Exercise Performance

a. Inspection Scope

The inspectors sampled licensee submittals for the Drill/Exercise Performance (DEP)performance indicator (PI) for the period from the second quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the DEP indicator in accordance with relevant procedures and the NEI guidance. Specifically, the inspectors reviewed licensee records and processes, including procedural guidance on assessing opportunities for the PI; assessments of PI opportunities during pre-designated control room simulator training sessions; performance during the 2016 biennial exercise; and performance during other drills. Specific documents reviewed are listed in the Attachment to this report.

This inspection constitutes one DEP sample as defined in IP 71151.

b. Findings

No findings were identified.

.2 Emergency Response Organization Readiness

a. Inspection Scope

The inspectors sampled licensee submittals for the ERO Drill Participation PI for the period from the second quarter of 2016 through the second quarter of 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures, and NEI guidance. Specifically, the inspectors reviewed licensee records and processes, including procedural guidance on assessing opportunities for the PI; performance during the 2016 biennial exercise; and other drills; and revisions of the roster of personnel assigned to key ERO positions. Specific documents reviewed are listed in the Attachment to this report.

This inspection constitutes one ERO drill participation sample as defined in IP 71151.

b. Findings

No findings were identified.

.3 Alert and Notification System Reliability

a. Inspection Scope

The inspectors sampled licensee submittals for the ANS PI for the period from the second quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, were used. The inspectors reviewed the licensees records associated with the PI to verify that the licensee accurately reported the indicator in accordance with relevant procedures and the NEI Guidance. Specifically, the inspectors reviewed licensee records and processes including procedural guidance on assessing opportunities for the PI and results of periodic ANS operability tests. Specific documents reviewed are listed in the Attachment to this report.

This inspection constitutes one ANS sample as defined in IP 71151.

b. Findings

No findings were identified.

.4 Mitigating Systems Performance IndexHigh Pressure Injection System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - High Pressure Injection System PI for the period from the third quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, event reports and NRC Integrated IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI high pressure injection system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

.5 Mitigating Systems Performance IndexResidual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System PI for the period from the third quarter 2016 through the second quarter 2017.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, CRs, MSPI derivation reports, event reports and NRC IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI residual heat removal system sample as defined in IP 71151-05.

b. Findings

No findings were identified.

.6 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Leakage PI for the period from the third quarter 2016 through the second quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, RCS leakage tracking data, CRs, event reports and NRC IRs for the period of the third quarter 2016 through the second quarter 2017 to validate the accuracy of the submittals. The inspectors also reviewed the licensees CR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one reactor coolant system leakage sample as defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees corrective action program at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensees corrective action program as a result of the inspectors observations; however, they are not discussed in this report.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues: 1-2 Diesel Generator Issues Resulting in

Additional Inoperability

a. Inspection Scope

The inspectors selected the following condition reports for in-depth review:

  • CR-PLP-2017-00609, Received Alarm EK-0555, Diesel Generator Breaker 152-213 Trip, Unexpectedly;

Between January 2017 and July 2017, the licensee initiated multiple condition reports involving the 1-2 DG for issues that resulted in additional inoperability of the system.

The inspectors reviewed these condition reports and their associated work orders.

As appropriate, the inspectors verified the following attributes during their review of the licensee's corrective actions for the above condition reports and other related condition reports:

  • complete and accurate identification of the problem in a timely manner commensurate with its safety significance and ease of discovery;
  • consideration of the extent of condition, generic implications, common cause, and previous occurrences;
  • evaluation and disposition of operability/functionality/reportability issues;
  • classification and prioritization of the resolution of the problem commensurate with safety significance;
  • identification of the apparent and contributing causes of the problem; and
  • identification of corrective actions, which were appropriately focused to correct the problem;
  • completion of corrective actions in a timely manner commensurate with the safety significance of the issue; and
  • evaluation of the applicability for operating experience and communication of applicable lessons learned to appropriate organizations.

The inspectors discussed the corrective actions and associated evaluations with licensee personnel.

This review constituted one in-depth problem identification and resolution inspection sample as defined in IP 71152.

b. Observations and Assessments The inspectors reviewed the adverse condition analyses (ACA) associated with CR-PLP-2017-00609 and CR-PLP-2017-02655, and the disposition associated with CR-PLP-2017-01291. The inspectors did not identify any significant issues associated with the licensees CAP processes for these condition reports. However, the inspectors noted the licensees conclusions in the ACA associated with CR-PLP-2017-02655.

The licensees ACA for the issue identified in CR-PLP-2017-02655, which occurred on May 23, 2017, discussed previous occurrences of similar failures. On May 23, 2017, during performance a monthly surveillance test on the 1-2 DG, the P-18A fuel oil transfer pump would not stop auto-filling the 1-2 DG fuel oil day tank. The licensee manually stopped the pump and, although the 1-2 DG was already inoperable due to the surveillance test, declared the 1-2 DG inoperable due to the P-18A auto-fill function not operating as expected. The licensee performed troubleshooting and identified that LS-1453, the 1-2 DG fuel oil day tank low level switch, contacts did not open as expected when sufficient level in the 1-2 DG fuel oil day tank was reached. As a result of this condition, the P-18A fuel oil transfer pump did not stop auto-filling as anticipated.

Through troubleshooting the licensee identified that the probable cause was binding due to air entrapment of the level switch float in the upper portion of the float chamber. The resulting actions were to adjust the level switch mechanism to prevent air entrapment in LS-1453.

The ACA discussed similar failures of level switch LS-1453 that had occurred on four other occasions since 2013. An apparent cause evaluation (ACE) was performed for one of these failures on May 18, 2015. In this case, when the automatic fill function for the 1-2 DG fuel oil day tank was placed into service, P-18A started to fill the tank, even though tank level was sufficient and the operators expected P-18A to remain off. The licensee determined the cause of the event to be contact between the level switch and a seismic support for the tank, which resulted in binding due to a misalignment of the internal float in LS-1453. Additionally, it was discussed in the ACE that, due to the contact, the level switch and associated piping was not plumb. This was identified as a legacy issue associated with inadequate understanding of the impact of interference when the level switch was installed. For this event, the level switch internals were modified to eliminate the binding. Additionally, a corrective action was created to evaluate rework of the piping for the level switch and eliminate the contact with the seismic support. It was decided that the piping rework was an enhancement action and no active rework of the piping was pursued.

Two of the similar failures occurred in January 2017 and April 2017. In each of these instances, the licensee identified possible failure mechanisms and implemented corrective actions to restore operability. However, the licensee determined, for these events, that there were several possible causes that could not be eliminated through the troubleshooting process. The ACA identified that corrective actions in the previous events did not adequately eliminate the identified possible failure mechanisms. The identified possible failure mechanisms were mitigated, but not eliminated completely.

The inspectors noted that the ACA also discussed that rework of the level switch piping, which was identified as an enhancement in 2015, would eliminate all possible causes.

The licensees corrective action to rework the level switch piping and replace LS-1453 was completed on July 28, 2017. This resulted in the assurance that the level switch piping was plumb and the contact between LS-1453 and the seismic support was eliminated.

c. Findings

Introduction:

A finding of very low safety significance (Green) and an associated non-cited violation (NCV) of TS 5.4.1, Procedures, was self-revealed on March 31, 2017, when the 1-2 DG tripped during performance of monthly TS surveillance procedure MO-7A-2, Emergency Diesel Generator 1-2. Specifically, during conduct of the monthly surveillance procedure, restoration activities associated with maintenance of breaker 152-213, 1-2 DG to Bus 1D, were being performed. When maintenance personnel closed the trip cutouts for the Z-phase of the 1-2 DG differential overcurrent relay, an unbalanced current flow into the differential relay resulted in relay actuation. This actuation resulted in a trip of the output breaker and subsequently a trip of the 1-2 DG. The trip caused a delay in the TS surveillance activities, and resulted in extended unavailability and inoperability of the 1-2 DG.

Description:

On March 31, 2017, the monthly TS surveillance procedure for the 1-2 DG was scheduled to start at 12:00 p.m. The preventive maintenance associated with the 1-2 DG differential overcurrent relay was scheduled to end at 1:00 p.m. This indicated to operators that these work activities were not bound by any logic tie and the activities could be overlapped.

When maintenance personnel performing the maintenance activities associated with the relay work identified that the 1-2 DG was running, they requested permission from the control room to place the Z-phase differential relay back into service prior to closing breaker 152-213, 1-2 DG to Bus 1D output breaker. The operators informed the maintenance personnel that they could return the relay to service when breaker 152-213 was closed. Once breaker 152-213 was closed during the surveillance procedure, the maintenance workers were restoring the relay when it tripped, causing breaker 152-213 and the 1-2 DG to trip. The maintenance personnel immediately informed the control room of their activities and promptly revealed the cause of the DG trip. This sequence of events caused additional inoperability and unavailability time of the 1-2 DG due to time taken for evaluation of the trip and re-performing the surveillance test. Prior to the start of the surveillance test, the licensee had declared the 1-2 DG inoperable and appropriately entered TS 3.8.1, Condition B. The licensee restored the differential overcurrent trip relay circuitry and successfully re-performed the test. Once those activities were completed, the DG was declared operable.

As discussed in the licensees disposition evaluation for this issue, this event was directly caused by restoration of the differential relay while the DG output breaker was closed. The engineering staff identified that the differential relay properly actuated as designed, which resulted in the trip of the 1-2 DG. As corrective actions, the licensee updated work instructions associated with the differential overcurrent relays to include caution statements that opening or closing trip cutouts for the differential relays while the output breakers from the DGs to the associated buses were closed could cause the differential relays to actuate.

Analysis:

The inspectors determined that the failure to adequately pre-plan and perform maintenance that could affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances was contrary to the requirements of TS 5.4.1, Procedures, and was a performance deficiency warranting further review.

The performance deficiency was determined to be more than minor, and thus a finding, in accordance with IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, because it was associated with the Mitigating Systems cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

The inspectors determined the finding could be evaluated using the Significance Determination Process in accordance with IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, dated June 19, 2012. The inspectors reviewed the Mitigating Systems Screening Questions in Appendix A, Exhibit 2 and answered No to all questions. As a result, the finding was determined to be very of low safety significance (Green).

This finding had a cross-cutting aspect in the area of Human Performance, in the Work Management aspect, for the failure to identify and manage risk commensurate to the work. Specifically, the licensee committed a human performance error by failing to adequately plan, control, and execute electrical maintenance activities associated with the 1-2 DG during the monthly TS surveillance test of the DG. The licensee did not appropriately assess and coordinate the work activities of different work groups to address the impact of those work activities on the plant, which resulted in the 1-2 DG being inoperable longer than planned (H.5).

Enforcement:

TS Section 5.4.1 states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978.

NRC Regulatory Guide 1.33, Appendix A, Section 9a, states, in part, that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to the above, on March 31, 2017, while performing monthly TS surveillance procedure MO-7A-2, Emergency Diesel Generator 1-2, in conjunction with electrical maintenance procedure WI-SPS-E-09, Calibration of Bus 1D Protective Relays, the licensee failed to properly pre-plan and perform maintenance that affected the 1-2 DG by failing to understand the impact of restoration of the Z-phase differential overcurrent relay while the 1-2 DG output breaker was closed. Specifically, performance of these two activities in conjunction with each other resulted in unbalanced current flow into the differential relay and a trip of the 1-2 DG. The issue was entered into the licensees CAP as CR-PLP-2017-01291, While Performing MO-7A-2, Breaker 152-213 Opened and K-6B, Emergency Diesel Generator 1-2, Tripped.

Because this violation was of very low safety significance and it was entered into the licensees CAP as CR-PLP-2017-01291, this violation is being treated as a NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000255/2017003-03, 1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG)

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 (Closed) Licensee Event Report 05000255/2017002-00: Reactor Protection System

Actuation While the Reactor was Shutdown On May 19, 2017, an unexpected actuation of the RPS occurred during the performance of procedure PO-1, Operations Pre-Startup Tests. While testing the function of RPS actuation from a loss of main generator load input signal, the operator performing the test incorrectly determined MOD-389, the Main Generator Motor-Operated Disconnect, to be open when it was actually closed. The PO-1 procedure required that either MOD-389 be in the open position or that the main generator protective trip circuitry be bypassed. Because the operator incorrectly determined the state of the motor-operated disconnect, the aforementioned conditional step was erroneously performed, and the main generator protective trip circuitry was not bypassed as required, leading to the unplanned RPS actuation. At the time of the actuation, the reactor was shutdown in Mode 5 with all control rods inserted and the RPS responded as expected for the plant conditions. The operator was given remediation training and enhancements to procedure guidance were briefed to all operating crews on the execution of conditional steps. Also, the licensee increased required behavioral observations and supervisory oversight within the operations department.

The inspectors determined that the failure of the operator to correctly perform procedure PO-1, Operations Pre-Startup Tests, constituted a performance deficiency and that this performance deficiency was similar to Example 4.b of IMC 0612, Appendix E, Examples of Minor Issues. For this issue, the unexpected RPS actuation produced a valid RPS signal for a reactor trip. However, the trip did not result in any upset to plant stability since control rods were fully inserted due to the plant being shutdown.

Therefore, the failure to follow the RPS testing procedure constituted a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. This licensee event report (LER) is closed.

Documents reviewed are listed in the Attachment to this report.

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA6 Management Meetings

.1 Exit Meeting Summary

On October 18, 2017, the inspectors presented the inspection results to Mr. C. Arnone, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • the inspection results of the Emergency Preparedness Program with Mr. C. Arnone, Site Vice President, and licensee staff on July 20, 2017; and
  • the inspection results for the Radiation Safety Program review with Mr. D. Corbin, General Manager Plant Operations, and licensee staff on July 14, 2017.

The inspectors confirmed that none of the potential report input discussed was considered proprietary. Proprietary material received during the inspection was returned to the licensee.

4OA7 Licensee-Identified Violations

The following licensee-identified violation of U.S. Nuclear Regulatory Commission requirements was determined to be of very low safety significance or Severity Level IV and meet the U.S. Nuclear Regulatory Commission Enforcement Policy criteria for being dispositioned as a Non-Cited Violation.

  • The licensee identified a finding of very low safety significance (Green) and an associated NCV of TS 5.7.2, which requires, in part, that each entryway into High Radiation Areas (HRAs) with dose rates greater than 1.0 rem/hour at 30 centimeters from the radiation source or any surface penetrated by the radiation, but less than 500 rads/hour at 1 meter from the radiation source or from any surface penetrated by the radiation source shall be provided with a locked or continuously guarded door or gate that prevents unauthorized entry. Contrary to the above, on May 4, 2017, the licensee failed to lock or continuously guard an entryway into a HRA with dose rates greater than 1.0 rem/hour at 30 centimeters from the radiation source or any surface penetrated by the radiation, but less than 500 rads/hour at 1 meter from the radiation source or from any surface penetrated by the radiation source. Specifically, an entryway was left unguarded when the individual assigned to guard the entryway left the area prior to another guard being stationed. This issue was identified by a radiation protection technician who immediately stationed another guard. This issue was entered into the licensees CAP as CR-PL-2017-02160.

The failure to continuously guard the HRA entryway was a performance deficiency that was within the licensees ability to foresee and should have been prevented. The performance deficiency was more than minor because it was associated with the Program and Process attribute of the Occupational Radiation Safety cornerstone and adversely affected the cornerstone objective of ensuring the adequate protection of worker health and safety from exposure to radiation.

The finding was determined to be of very low safety significance (Green)because it did not involve as-low-as-reasonably-achievable planning or work controls, there was no overexposure or substantial potential for an overexposure, and the licensees ability to assess dose was not compromised.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

C. Arnone, Site Vice President
D. Corbin, General Manager Plant Operations
B. Baker, Operations Manager - Shift
J. Borah, Engineering Manager, Systems and Components
T. Davis, Regulatory Assurance
N. DeMaster, Outage Manager
B. Dotson, Regulatory Assurance
J. Erickson, Regulatory Assurance
O. Gustafson, Director of Regulatory and Performance Improvement
J. Hardy, Regulatory Assurance Manager
J. Haumersen, Site Projects and Maintenance Services Manager
G. Heisterman, Maintenance Manager
K. Howard, Emergency Preparedness Specialist
M. Lee, Operations Manager - Support
D. Lucy, Production Manager
D. Malone, Emergency Planning Manager
T. Mulford, Operations Manager
W. Nelson, Training Manager
D. Nestle, Radiation Protection Manager
C. Plachta, Nuclear Independent Oversight Manager
M. Mylnarek, Nuclear Independent Oversight Manager
K. OConnor, Site Engineering Director
M. Schultheis, Performance Improvement Manager
M. Soja, Chemistry Manager
J. Tharp, Security Manager

U.S. Nuclear Regulatory Commission

E. Duncan, Chief, Reactor Projects Branch 3

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000255/2017003-01 URI Left Train Emergency Diesel Generator Load Sequencer Failure (Section 1R19.1.b)
05000255/2017003-02 URI Cause of 42-2/RPS Breaker Failure to Open (Section 1R19.1.c)
05000255/2017003-03 NCV 1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG (Section 4OA2.2.c)

Closed

05000255/2017002-00 LER Reactor Protection System Actuation While the Reactor was Shutdown (Section 4OA3.1)
05000255/2017003-03 NCV 1-2 Diesel Generator Trip During Maintenance Resulting in Additional Unavailability of the 1-2 DG (Section 4OA2.2.c)

Discussed

None

LIST OF DOCUMENTS REVIEWED