ML17334A425: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(4 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 09/07/1982
| issue date = 09/07/1982
| title = Documents Discussions on Request for License Amend Granting Relief from Requirements of Tech Spec 3.5.2 Re Safety Injection Pump Out of Svc.Safety Evaluation Prepared in Conjunction W/Westinghouse Supports Relief Request
| title = Documents Discussions on Request for License Amend Granting Relief from Requirements of Tech Spec 3.5.2 Re Safety Injection Pump Out of Svc.Safety Evaluation Prepared in Conjunction W/Westinghouse Supports Relief Request
| author name = JURGENSEN R W
| author name = Jurgensen R
| author affiliation = AMERICAN ELECTRIC POWER SERVICE CORP.
| author affiliation = AMERICAN ELECTRIC POWER SERVICE CORP.
| addressee name = DENTON H R, VARGA S A
| addressee name = Denton H, Varga S
| addressee affiliation = NRC, NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR)
| addressee affiliation = NRC, NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR)
| docket = 05000315
| docket = 05000315
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:~~ANEPICANELECTR1CPGWERSe>viceCorpo~etio)s2Broadu:ay.
{{#Wiki_filter:~                                           ~
Xeu:Pork,.l.}.Ir)00.t(2/2p.S>0.9000September 7,1982AEP:NRC:0739 DonaldC.CookNuclearPlantUnitNo.1DocketNo.50-315LicenseNo.DPR-58REQUESTFORRELIEFFROMTECHNICAL SPECIFICATION 3.5.2Mr.HaroldR.Denton,DirectorOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission Washington, D.C.20555Attention:
ANEPICAN ELECTR1C PGWER                              Se> vice Corpo~ etio)s 2 Broadu:ay. Xeu: Pork,.l. }. Ir)00.t (2 /2p .S > 0. 9000 September    7, 1982 AEP:NRC:0739 Donald C. Cook Nuclear Plant      Unit    No.     1 Docket No. 50-315 License No. DPR-58 REQUEST FOR RELIEF FROM TECHNICAL SPECIFICATION                 3.5.2 Mr. Harold R. Denton, Director Of fice of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Mr. Steven A. 'Varga
Mr.StevenA.'Varga


==DearMr.Denton:==
==Dear Mr. Denton:==
Thisletterdocuments thediscussions heldwithmembersofyourStaffconcerning ourrequestforalicenseamendment grantingrelieffromtherequirements of.Technical Specification 3.5.2.EachUnitoftheCookNuclearPlanthastwoSafetyInjection PumpsplustwoCentrifugal ChargingPumpsandtwoResidualHeatRemovalPumps.Inpreparation fortheblackouttestperformed onAugust14,1982,UnitNo.1'sNorthSafetyInjection Pumpsufferedseveredamage.We",haveproceeded torepairthepumpexpeditiously buthavenotbeenabletocompletetherepairsasofthetimeofthisletter.UnitNo.1Technical Specification (T/S)No.3.5.2requires, amongotherthings,thattwoSafetyInjection (SI)PumpsbeoperableinModes1,2and3.UnitNo.1iscurrently
 
'completing itsrefueling outageandthereturntoModes3,2and1isprevented bytheinoperability oftheSIpumpandtheT/Smentioned above.Inordertoproceedwiththelowpowerphysicstesting,werequestawaiveroftherequirement tohavetwoSIpumpsoperableinModes2(reactorthermalpowerlessthanorequalto5%)and3foraperiodofoneweekbeginning atthetimetheUnitentersMode3.TheSouthSIpumpwillbedemonstrated operablepriortoenteringMode3.Allremaining technical specification requirements willbemet.Attachment 1tothislettercontainsthesafetyevaluation preparedbyusinconjunction withWestinghouse.
This  letter  documents  the discussions held with members of your Staff concerning our request for        a license amendment granting relief from the requirements of .Technical Specification 3.5.2 .
Theconclusion isthatevenifweweretolosetheoperable1SSafetyInjection Pumpsufficient marginKP wy,@5"-&~9'M
Each Unit of the Cook Nuclear Plant has two Safety Injection Pumps plus  two Centrifugal Charging Pumps and two Residual Heat Removal Pumps.
~-'a wrMr.H.R.Dent.AEP:NRC:0739wouldstillexisttothelimitsspecified in10CFR50.46.Thus,thisreliefisnotdetrimental tothehealthandsafetyofthepublic.IWewouldappreciate theexpeditious handlingofthisrequestbyyourStaff.AEPSCinterprets 10CFR170.22asrequiring thataClassIIIAmendment Feebepaidforthechange.Acheckintheamountof$4,000willbetransmitted toyouinafutureletter.hThisTechnical Specification reliefrequesthasbeenreviewedbytheCookPlantPNSRC.ItwillbereviewedbyAEPSC'sNSDRCatthenext~scheduled meeting.Duetothisletterbeingwrittenonshortnotice,ithasnotbeenpreparedfollowing ourstanda"dCorporate Procedures forsuchletters.Weshall,however,reviewtheletteraccording toourCorporate Procedures andwil'nform youifanymodification isrequired.
In preparation for the blackout test performed on August 14, 1982, Unit No. 1's North Safety Injection Pump suffered severe damage. We
Verytrulyyours,/emcAttachment cc:JohnE.Dolan-ColumbusR.S.HunterM.P.AlexichW.G.Smith,Jr.-BridgmanR.C.CallenG.CharnoffJoeWilliams, Jr.NRCResidentInspector atCookPlant-Bridgman'~~
",have proceeded to repair the pump expeditiously but have not been able to complete the repairs as of the time of this letter. Unit No. 1 Technical Specification (T/S) No. 3.5.2 requires, among other things, that two Safety Injection (SI) Pumps be operable in Modes 1, 2 and 3.
Attachment toAEP:NRC:0739 LOCAEvaluation forD.C.CookUnit1withOneSafetInectionPumOutofServiceThepurposeofthisevaluation istoassesstheeffectofonesafetyinjection pumpoutofservicefortheCookUnit1NuclearPlantonLossofCoolantAccident(LOCA)consequences.
Unit No. 1 is currently 'completing its refueling outage and the return to Modes 3, 2 and 1 is prevented by the inoperability of the SI pump and the T/S mentioned above. In order to proceed with the low power physics testing, we request a waiver of the requirement to have two SI pumps operable in Modes 2 (reactor thermal power less than or equal to 5%) and 3 for a period of one week beginning at the time the Unit enters Mode 3.
Presently, theplantisfueledbyExxonNuclearCompany.However,theevaluation providedbelowisjudgedtobeapplicable tothenon'Westinghouse fuel,sincetherearenoknownmajordesigndifferences thatwouldhaveasignificant impactontheLOCAbehaviorimportant forthisevaluation.
The South SI pump will be demonstrated operable prior to entering Mode
LareBreakLOCASafetyinjection pumpflowprovidesaninsignificant proportion ofthetotalECCSflowduringalargebreakaccident, whereRCSpressurerapidlydropstonearatmospheric.
: 3. All remaining technical specification requirements will be met.
Accumulator andlowheadsafetyinjection (RHR)flowareimportant forthisaccident.
Attachment   1  to this  letter    contains the safety evaluation prepared by us in conjunction with Westinghouse.
Therefore, thelossofasafetyinjection pumphasanegligible effectonlargeLOCAcalculated peakcladtemperature.
we were to lose the operable 1S Safety The conclusion is that even    if K
SmallBreakLOCATheplant'sprotection againstsmallLOCAscomesfromatwotrainsystemincluding atotaloftwosafetyinjection pumpsandtwohighheadchargingpumps.SmallLOCAFSARlicensing analysesassumetheworstsinglefailuretobelossofatrain,leavingoneintermediate headSIpumpandonechargingpump.ThesmallLOCAanalysisyieldscladtemperatures wellbelow10CFR50.46limits.Thisanalysisassumption boundsthepresentplantconfiguration withonesafetyinjection pumpoutofserviceandnosinglefailure.Iftheworstsinglefailureassumption isconsidered inadditiontothe;lossofthesafetyinjection pump,andfurther,thetrainlostisassumed'tohavetheoperational safetyinjection pump,ECCSflowisdelivered fromonlythehighheadchargingpump.Thefollowing paragraphs evaluatethisscenario.
Injection  Pump  sufficient margin P
Reduction ofECCSflowintherangeof600to1200psiahasanadverse--"effect oncalculated cladtemperature forarangeofsmallLOCAbreaksizes.Thelossofasafetyinjectionpumphastheeffectofreducingdelivered ECCSflowinthatimportant pressurerange.TotalECCSflowwillbedegradedbyapproximately 56%averagedoverthispressureinterval.
 
Established sensitivity studieshaveindicated thatsuchadegradation resultsinasmuchasa550oFsmallLOCAPCTincrease.  
wy,
~~0t~.ThesmallbreakanalysisforCook1doesnotusethelatestNRCapprovedWsmallLOCAEvaluation Model.ThecurrentsmallbreakLOCAEMwouldcalculate aPCTofapproximately 1200oF,reducedfrom1493F,predicted bytheanalysisintheFSAR.ThisnewPCTisestablished fromanalysisofasubstantially equivalent plant(3250MWt,4Loop,sameSISdesign)analyzedinHCAP-8970-P-A,
    @5"-&~9'M~ 'a
,"Westinghouse Emergency CoreCo'olingSystemSmall8reakOctober,1975Model",andappliestoCook.Additionally, creditforconservative assumptions inthesmallLOCAFSARanalysiscanmitigatethePCTpenalty.Also,thecurrentsmallLOCAFSARanalysisisperformed at100%powerwhileduringtheperiodoftimeforwhichweareseekingT/Sreliefthereactorwillnotexceed5%power.Thelowerpower.levelof5%versus100%wouldmorethanoffsettheconsequences ofreducedECCSflow.Inconclusion, operation ofCook1withasafetyinjection pumpoutofserviceandamaximumpowerlevelof5%forabrief'periodoftimeisstillboundedbythesmallLOCAFSARanalysis.
 
Inaddition,thefactthatthepresentanalysishassignificant marginto10CFR50.46PCTlimitsindicates thatstartupoftheplantfromthisrefueling outageisnotasafetyconcern.}}
wr Mr. H. R. Dent   .                                             AEP: NRC: 0739 would  still exist  to the  limits specified in    10 CFR 50.46. Thus, this relief is  not detrimental to the health      and  safety of the public.
I We  would appreciate    the expeditious handling of this request by your  Staff.
AEPSC  interprets    10 CFR  170.22 as requiring that a Class    III Amendment Fee be    paid for the change.     A check in the amount of    $ 4,000 will be transmitted to you in a future        letter.h This  Technical Specification relief request        has been reviewed by the Cook Plant PNSRC.       It will be  reviewed by AEPSC's    NSDRC  at the next
  ~
scheduled meeting.
Due to this letter being written on short notice,         it has not been prepared following our standa"d Corporate Procedures for such letters.
We shall, however, review the letter according to our Corporate Procedures and wil'nform you        if any modification is required.
Very  truly yours,
    /emc Attachment cc:   John E. Dolan     - Columbus R. S. Hunter M. P. Alexich W. G. Smith, Jr. Bridgman R. C. Callen                                                                ' ~ ~
G. Charnoff Joe  Williams, Jr.
NRC  Resident Inspector at    Cook Plant  - Bridgman
 
Attachment to AEP:NRC:0739 LOCA  Evaluation for D. C. Cook Unit      1 with  One Safet    In ection Pum Out of Service The purpose    of this evaluation is to assess the effect of one safety injection pump out of service for the Cook Unit 1 Nuclear Plant on Loss of Coolant Accident (LOCA) consequences.           Presently, the plant is fueled by Exxon Nuclear Company.         However, the evaluation provided below is judged to be applicable to the non 'Westinghouse fuel, since there are no known major design differences that would have a significant impact on the LOCA behavior important for this evaluation.
Lar  e  Break  LOCA Safety injection      pump flow provides an insignificant proportion of the total ECCS  flow during    a large break accident, where RCS pressure rapidly drops to near atmospheric. Accumulator and low head safety injection (RHR) flow are important for this accident. Therefore, the loss of a safety injection pump has a negligible effect on large LOCA calculated peak clad temperature.
Small Break LOCA The  plant's protection against small LOCAs comes from a two train system including  a total of two safety injection pumps and two high head charging pumps. Small LOCA FSAR licensing analyses assume the worst single failure to be loss of a train, leaving one intermediate head SI pump and one charging pump. The small LOCA analysis yields clad temperatures well below 10    CFR  50.46    limits. This analysis assumption bounds the present plant configuration with        one  safety injection pump out of service and no single failure.
If  the worst single fai lure assumption is considered in addition to the
  ;loss of the safety injection pump, and further, the train lost is assumed
  'to have the operational safety injection pump, ECCS flow is delivered from only the high head charging pump. The following paragraphs evaluate this scenario.
Reduction of    ECCS flow in the range of 600 to 1200 psia has an adverse
--"effect   on calculated clad temperature for a range of small LOCA break sizes. The loss of a safety i njecti on pump has the effect of reducing delivered    ECCS  flow in that important pressure range.     Total ECCS flow will be    degraded    by  approximately 56% averaged over this pressure interval.
Established sensitivity studies have indicated that such a degradation results in as much as a 550oF small LOCA PCT increase.
 
~
0
  ~
t                  ~     .
The small break  analysis for Cook 1 does not use the latest NRC  approved W small LOCA Evaluation Model. The current small break LOCA EM would calculate a PCT  of approximately 1200oF, reduced from 1493 F, predicted by the analysis in the FSAR. This new PCT is established from analysis of a  substantially  equivalent plant (3250 MWt,4 Loop, same SI S design) analyzed in HCAP-8970-P-A, ,"Westinghouse Emergency Core Co'oling System Small 8reak October, 1975 Model", and applies to Cook.
Additionally, credit for conservative assumptions in the small LOCA FSAR analysis can mitigate the PCT penalty. Also, the current small LOCA FSAR analysis is performed at 100% power while during the period of time for which we are seeking T/S relief the reactor will not exceed 5% power.
The lower power. level of 5% versus 100% would more than offset the consequences of reduced ECCS flow.
In conclusion, operation of Cook 1 with a safety injection pump out of service and a maximum power level of 5% for a brief 'period of time is still bounded by the small LOCA FSAR analysis. In addi tion, the fact that the present analysis has significant margin to 10 CFR 50.46 PCT limits indicates that startup of the plant from this refueling outage is not a safety concern.}}

Latest revision as of 12:54, 22 October 2019

Documents Discussions on Request for License Amend Granting Relief from Requirements of Tech Spec 3.5.2 Re Safety Injection Pump Out of Svc.Safety Evaluation Prepared in Conjunction W/Westinghouse Supports Relief Request
ML17334A425
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 09/07/1982
From: Jurgensen R
AMERICAN ELECTRIC POWER SERVICE CORP.
To: Harold Denton, Varga S
NRC, Office of Nuclear Reactor Regulation
References
AEP:NRC:0739, AEP:NRC:739, NUDOCS 8209130234
Download: ML17334A425 (5)


Text

~ ~

ANEPICAN ELECTR1C PGWER Se> vice Corpo~ etio)s 2 Broadu:ay. Xeu: Pork,.l. }. Ir)00.t (2 /2p .S > 0. 9000 September 7, 1982 AEP:NRC:0739 Donald C. Cook Nuclear Plant Unit No. 1 Docket No. 50-315 License No. DPR-58 REQUEST FOR RELIEF FROM TECHNICAL SPECIFICATION 3.5.2 Mr. Harold R. Denton, Director Of fice of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Mr. Steven A. 'Varga

Dear Mr. Denton:

This letter documents the discussions held with members of your Staff concerning our request for a license amendment granting relief from the requirements of .Technical Specification 3.5.2 .

Each Unit of the Cook Nuclear Plant has two Safety Injection Pumps plus two Centrifugal Charging Pumps and two Residual Heat Removal Pumps.

In preparation for the blackout test performed on August 14, 1982, Unit No. 1's North Safety Injection Pump suffered severe damage. We

",have proceeded to repair the pump expeditiously but have not been able to complete the repairs as of the time of this letter. Unit No. 1 Technical Specification (T/S) No. 3.5.2 requires, among other things, that two Safety Injection (SI) Pumps be operable in Modes 1, 2 and 3.

Unit No. 1 is currently 'completing its refueling outage and the return to Modes 3, 2 and 1 is prevented by the inoperability of the SI pump and the T/S mentioned above. In order to proceed with the low power physics testing, we request a waiver of the requirement to have two SI pumps operable in Modes 2 (reactor thermal power less than or equal to 5%) and 3 for a period of one week beginning at the time the Unit enters Mode 3.

The South SI pump will be demonstrated operable prior to entering Mode

3. All remaining technical specification requirements will be met.

Attachment 1 to this letter contains the safety evaluation prepared by us in conjunction with Westinghouse.

we were to lose the operable 1S Safety The conclusion is that even if K

Injection Pump sufficient margin P

wy,

@5"-&~9'M~ 'a

wr Mr. H. R. Dent . AEP: NRC: 0739 would still exist to the limits specified in 10 CFR 50.46. Thus, this relief is not detrimental to the health and safety of the public.

I We would appreciate the expeditious handling of this request by your Staff.

AEPSC interprets 10 CFR 170.22 as requiring that a Class III Amendment Fee be paid for the change. A check in the amount of $ 4,000 will be transmitted to you in a future letter.h This Technical Specification relief request has been reviewed by the Cook Plant PNSRC. It will be reviewed by AEPSC's NSDRC at the next

~

scheduled meeting.

Due to this letter being written on short notice, it has not been prepared following our standa"d Corporate Procedures for such letters.

We shall, however, review the letter according to our Corporate Procedures and wil'nform you if any modification is required.

Very truly yours,

/emc Attachment cc: John E. Dolan - Columbus R. S. Hunter M. P. Alexich W. G. Smith, Jr. Bridgman R. C. Callen ' ~ ~

G. Charnoff Joe Williams, Jr.

NRC Resident Inspector at Cook Plant - Bridgman

Attachment to AEP:NRC:0739 LOCA Evaluation for D. C. Cook Unit 1 with One Safet In ection Pum Out of Service The purpose of this evaluation is to assess the effect of one safety injection pump out of service for the Cook Unit 1 Nuclear Plant on Loss of Coolant Accident (LOCA) consequences. Presently, the plant is fueled by Exxon Nuclear Company. However, the evaluation provided below is judged to be applicable to the non 'Westinghouse fuel, since there are no known major design differences that would have a significant impact on the LOCA behavior important for this evaluation.

Lar e Break LOCA Safety injection pump flow provides an insignificant proportion of the total ECCS flow during a large break accident, where RCS pressure rapidly drops to near atmospheric. Accumulator and low head safety injection (RHR) flow are important for this accident. Therefore, the loss of a safety injection pump has a negligible effect on large LOCA calculated peak clad temperature.

Small Break LOCA The plant's protection against small LOCAs comes from a two train system including a total of two safety injection pumps and two high head charging pumps. Small LOCA FSAR licensing analyses assume the worst single failure to be loss of a train, leaving one intermediate head SI pump and one charging pump. The small LOCA analysis yields clad temperatures well below 10 CFR 50.46 limits. This analysis assumption bounds the present plant configuration with one safety injection pump out of service and no single failure.

If the worst single fai lure assumption is considered in addition to the

loss of the safety injection pump, and further, the train lost is assumed

'to have the operational safety injection pump, ECCS flow is delivered from only the high head charging pump. The following paragraphs evaluate this scenario.

Reduction of ECCS flow in the range of 600 to 1200 psia has an adverse

--"effect on calculated clad temperature for a range of small LOCA break sizes. The loss of a safety i njecti on pump has the effect of reducing delivered ECCS flow in that important pressure range. Total ECCS flow will be degraded by approximately 56% averaged over this pressure interval.

Established sensitivity studies have indicated that such a degradation results in as much as a 550oF small LOCA PCT increase.

~

0

~

t ~ .

The small break analysis for Cook 1 does not use the latest NRC approved W small LOCA Evaluation Model. The current small break LOCA EM would calculate a PCT of approximately 1200oF, reduced from 1493 F, predicted by the analysis in the FSAR. This new PCT is established from analysis of a substantially equivalent plant (3250 MWt,4 Loop, same SI S design) analyzed in HCAP-8970-P-A, ,"Westinghouse Emergency Core Co'oling System Small 8reak October, 1975 Model", and applies to Cook.

Additionally, credit for conservative assumptions in the small LOCA FSAR analysis can mitigate the PCT penalty. Also, the current small LOCA FSAR analysis is performed at 100% power while during the period of time for which we are seeking T/S relief the reactor will not exceed 5% power.

The lower power. level of 5% versus 100% would more than offset the consequences of reduced ECCS flow.

In conclusion, operation of Cook 1 with a safety injection pump out of service and a maximum power level of 5% for a brief 'period of time is still bounded by the small LOCA FSAR analysis. In addi tion, the fact that the present analysis has significant margin to 10 CFR 50.46 PCT limits indicates that startup of the plant from this refueling outage is not a safety concern.