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| issue date = 09/07/1982
| issue date = 09/07/1982
| title = Documents Discussions on Request for License Amend Granting Relief from Requirements of Tech Spec 3.5.2 Re Safety Injection Pump Out of Svc.Safety Evaluation Prepared in Conjunction W/Westinghouse Supports Relief Request
| title = Documents Discussions on Request for License Amend Granting Relief from Requirements of Tech Spec 3.5.2 Re Safety Injection Pump Out of Svc.Safety Evaluation Prepared in Conjunction W/Westinghouse Supports Relief Request
| author name = JURGENSEN R W
| author name = Jurgensen R
| author affiliation = AMERICAN ELECTRIC POWER SERVICE CORP.
| author affiliation = AMERICAN ELECTRIC POWER SERVICE CORP.
| addressee name = DENTON H R, VARGA S A
| addressee name = Denton H, Varga S
| addressee affiliation = NRC, NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR)
| addressee affiliation = NRC, NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR)
| docket = 05000315
| docket = 05000315
Line 14: Line 14:
| page count = 5
| page count = 5
| project =  
| project =  
| stage = Approval
| stage = Request
}}
}}


=Text=
=Text=
{{#Wiki_filter:~~ANEPICAN ELECTR1C PGWER Se>vice Corpo~etio)s 2 Broadu:ay.
{{#Wiki_filter:~                                           ~
Xeu: Pork,.l.}.Ir)00.t (2/2p.S>0.9000 September 7, 1982 AEP:NRC:0739 Donald C.Cook Nuclear Plant Unit No.1 Docket No.50-315 License No.DPR-58 REQUEST FOR RELIEF FROM TECHNICAL SPECIFICATION 3.5.2 Mr.Harold R.Denton, Director Of fice of Nuclear Reactor Regulation U.S.Nuclear Regulatory Commission Washington, D.C.20555 Attention:
ANEPICAN ELECTR1C PGWER                               Se> vice Corpo~ etio)s 2 Broadu:ay. Xeu: Pork,.l. }. Ir)00.t (2 /2p .S > 0. 9000 September     7, 1982 AEP:NRC:0739 Donald C. Cook Nuclear Plant       Unit   No.     1 Docket No. 50-315 License No. DPR-58 REQUEST FOR RELIEF FROM TECHNICAL SPECIFICATION                 3.5.2 Mr. Harold R. Denton, Director Of fice of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Mr. Steven A. 'Varga
Mr.Steven A.'Varga  


==Dear Mr.Denton:==
==Dear Mr. Denton:==
This letter documents the discussions held with members of your Staff concerning our request for a license amendment granting relief from the requirements of.Technical Specification 3.5.2.Each Unit of the Cook Nuclear Plant has two Safety Injection Pumps plus two Centrifugal Charging Pumps and two Residual Heat Removal Pumps.In preparation for the blackout test performed on August 14, 1982, Unit No.1's North Safety Injection Pump suffered severe damage.We",have proceeded to repair the pump expeditiously but have not been able to complete the repairs as of the time of this letter.Unit No.1 Technical Specification (T/S)No.3.5.2 requires, among other things, that two Safety Injection (SI)Pumps be operable in Modes 1, 2 and 3.Unit No.1 is currently'completing its refueling outage and the return to Modes 3, 2 and 1 is prevented by the inoperability of the SI pump and the T/S mentioned above.In order to proceed with the low power physics testing, we request a waiver of the requirement to have two SI pumps operable in Modes 2 (reactor thermal power less than or equal to 5%)and 3 for a period of one week beginning at the time the Unit enters Mode 3.The South SI pump will be demonstrated operable prior to entering Mode 3.All remaining technical specification requirements will be met.Attachment 1 to this letter contains the safety evaluation prepared by us in conjunction with Westinghouse.
 
The conclusion is that even if we were to lose the operable 1S Safety Injection Pump sufficient margin K P wy,@5"-&~9'M~-'a wr Mr.H.R.Dent.AEP: NRC: 0739 would still exist to the limits specified in 10 CFR 50.46.Thus, this relief is not detrimental to the health and safety of the public.I We would appreciate the expeditious handling of this request by your Staff.AEPSC interprets 10 CFR 170.22 as requiring that a Class III Amendment Fee be paid for the change.A check in the amount of$4,000 will be transmitted to you in a future letter.h This Technical Specification relief request has been reviewed by the Cook Plant PNSRC.It will be reviewed by AEPSC's NSDRC at the next~scheduled meeting.Due to this letter being written on short notice, it has not been prepared following our standa"d Corporate Procedures for such letters.We shall, however, review the letter according to our Corporate Procedures and wil'nform you if any modification is required.Very truly yours,/emc Attachment cc: John E.Dolan-Columbus R.S.Hunter M.P.Alexich W.G.Smith, Jr.-Bridgman R.C.Callen G.Charnoff Joe Williams, Jr.NRC Resident Inspector at Cook Plant-Bridgman'~~
This letter   documents the discussions held with members of your Staff concerning our request for         a license amendment granting relief from the requirements of .Technical Specification 3.5.2 .
Attachment to AEP:NRC:0739 LOCA Evaluation for D.C.Cook Unit 1 with One Safet In ection Pum Out of Service The purpose of this evaluation is to assess the effect of one safety injection pump out of service for the Cook Unit 1 Nuclear Plant on Loss of Coolant Accident (LOCA)consequences.
Each Unit of the Cook Nuclear Plant has two Safety Injection Pumps plus two Centrifugal Charging Pumps and two Residual Heat Removal Pumps.
Presently, the plant is fueled by Exxon Nuclear Company.However, the evaluation provided below is judged to be applicable to the non'Westinghouse fuel, since there are no known major design differences that would have a significant impact on the LOCA behavior important for this evaluation.
In preparation for the blackout test performed on August 14, 1982, Unit No. 1's North Safety Injection Pump suffered severe damage. We
Lar e Break LOCA Safety injection pump flow provides an insignificant proportion of the total ECCS flow during a large break accident, where RCS pressure rapidly drops to near atmospheric.
",have proceeded to repair the pump expeditiously but have not been able to complete the repairs as of the time of this letter. Unit No. 1 Technical Specification (T/S) No. 3.5.2 requires, among other things, that two Safety Injection (SI) Pumps be operable in Modes 1, 2 and 3.
Accumulator and low head safety injection (RHR)flow are important for this accident.Therefore, the loss of a safety injection pump has a negligible effect on large LOCA calculated peak clad temperature.
Unit No. 1 is currently 'completing its refueling outage and the return to Modes 3, 2 and 1 is prevented by the inoperability of the SI pump and the T/S mentioned above. In order to proceed with the low power physics testing, we request a waiver of the requirement to have two SI pumps operable in Modes 2 (reactor thermal power less than or equal to 5%) and 3 for a period of one week beginning at the time the Unit enters Mode 3.
Small Break LOCA The plant's protection against small LOCAs comes from a two train system including a total of two safety injection pumps and two high head charging pumps.Small LOCA FSAR licensing analyses assume the worst single failure to be loss of a train, leaving one intermediate head SI pump and one charging pump.The small LOCA analysis yields clad temperatures well below 10 CFR 50.46 limits.This analysis assumption bounds the present plant configuration with one safety injection pump out of service and no single failure.If the worst single fai lure assumption is considered in addition to the;loss of the safety injection pump, and further, the train lost is assumed'to have the operational safety injection pump, ECCS flow is delivered from only the high head charging pump.The following paragraphs evaluate this scenario.Reduction of ECCS flow in the range of 600 to 1200 psia has an adverse--"effect on calculated clad temperature for a range of small LOCA break sizes.The loss of a safety i njecti on pump has the effect of reducing delivered ECCS flow in that important pressure range.Total ECCS flow will be degraded by approximately 56%averaged over this pressure interval.Established sensitivity studies have indicated that such a degradation results in as much as a 550oF small LOCA PCT increase.  
The South SI pump will be demonstrated operable prior to entering Mode
~~0 t~.The small break analysis for Cook 1 does not use the latest NRC approved W small LOCA Evaluation Model.The current small break LOCA EM would calculate a PCT of approximately 1200oF, reduced from 1493 F, predicted by the analysis in the FSAR.This new PCT is established from analysis of a substantially equivalent plant (3250 MWt,4 Loop, same SI S design)analyzed in HCAP-8970-P-A, ,"Westinghouse Emergency Core Co'oling System Small 8reak October, 1975 Model", and applies to Cook.Additionally, credit for conservative assumptions in the small LOCA FSAR analysis can mitigate the PCT penalty.Also, the current small LOCA FSAR analysis is performed at 100%power while during the period of time for which we are seeking T/S relief the reactor will not exceed 5%power.The lower power.level of 5%versus 100%would more than offset the consequences of reduced ECCS flow.In conclusion, operation of Cook 1 with a safety injection pump out of service and a maximum power level of 5%for a brief'period of time is still bounded by the small LOCA FSAR analysis.In addi tion, the fact that the present analysis has significant margin to 10 CFR 50.46 PCT limits indicates that startup of the plant from this refueling outage is not a safety concern.}}
: 3. All remaining technical specification requirements will be met.
Attachment   1 to this letter   contains the safety evaluation prepared by us in conjunction with Westinghouse.
we were to lose the operable 1S Safety The conclusion is that even    if K
Injection Pump   sufficient margin P
 
wy,
    @5"-&~9'M~ 'a
 
wr Mr. H. R. Dent   .                                             AEP: NRC: 0739 would still exist   to the   limits specified in     10 CFR 50.46. Thus, this relief is   not detrimental to the health     and safety of the public.
I We   would appreciate   the expeditious handling of this request by your Staff.
AEPSC interprets   10 CFR 170.22 as requiring that a Class     III Amendment Fee be   paid for the change.     A check in the amount of     $ 4,000 will be transmitted to you in a future       letter.h This Technical Specification relief request       has been reviewed by the Cook Plant PNSRC.       It will be reviewed by AEPSC's   NSDRC at the next
  ~
scheduled meeting.
Due to this letter being written on short notice,         it has not been prepared following our standa"d Corporate Procedures for such letters.
We shall, however, review the letter according to our Corporate Procedures and wil'nform you         if any modification is required.
Very truly yours,
    /emc Attachment cc:   John E. Dolan     - Columbus R. S. Hunter M. P. Alexich W. G. Smith, Jr. Bridgman R. C. Callen                                                                 ' ~ ~
G. Charnoff Joe Williams, Jr.
NRC Resident Inspector at     Cook Plant   - Bridgman
 
Attachment to AEP:NRC:0739 LOCA Evaluation for D. C. Cook Unit       1 with One Safet   In ection Pum Out of Service The purpose     of this evaluation is to assess the effect of one safety injection pump out of service for the Cook Unit 1 Nuclear Plant on Loss of Coolant Accident (LOCA) consequences.           Presently, the plant is fueled by Exxon Nuclear Company.         However, the evaluation provided below is judged to be applicable to the non 'Westinghouse fuel, since there are no known major design differences that would have a significant impact on the LOCA behavior important for this evaluation.
Lar e Break   LOCA Safety injection     pump flow provides an insignificant proportion of the total ECCS   flow during     a large break accident, where RCS pressure rapidly drops to near atmospheric. Accumulator and low head safety injection (RHR) flow are important for this accident. Therefore, the loss of a safety injection pump has a negligible effect on large LOCA calculated peak clad temperature.
Small Break LOCA The plant's protection against small LOCAs comes from a two train system including   a total of two safety injection pumps and two high head charging pumps. Small LOCA FSAR licensing analyses assume the worst single failure to be loss of a train, leaving one intermediate head SI pump and one charging pump. The small LOCA analysis yields clad temperatures well below 10   CFR 50.46   limits. This analysis assumption bounds the present plant configuration with       one safety injection pump out of service and no single failure.
If the worst single fai lure assumption is considered in addition to the
  ;loss of the safety injection pump, and further, the train lost is assumed
  'to have the operational safety injection pump, ECCS flow is delivered from only the high head charging pump. The following paragraphs evaluate this scenario.
Reduction of     ECCS flow in the range of 600 to 1200 psia has an adverse
--"effect   on calculated clad temperature for a range of small LOCA break sizes. The loss of a safety i njecti on pump has the effect of reducing delivered   ECCS   flow in that important pressure range.     Total ECCS flow will be   degraded   by approximately 56% averaged over this pressure interval.
Established sensitivity studies have indicated that such a degradation results in as much as a 550oF small LOCA PCT increase.
 
~
0
  ~
t                   ~     .
The small break   analysis for Cook 1 does not use the latest NRC approved W small LOCA Evaluation Model. The current small break LOCA EM would calculate a PCT   of approximately 1200oF, reduced from 1493 F, predicted by the analysis in the FSAR. This new PCT is established from analysis of a substantially equivalent plant (3250 MWt,4 Loop, same SI S design) analyzed in HCAP-8970-P-A, ,"Westinghouse Emergency Core Co'oling System Small 8reak October, 1975 Model", and applies to Cook.
Additionally, credit for conservative assumptions in the small LOCA FSAR analysis can mitigate the PCT penalty. Also, the current small LOCA FSAR analysis is performed at 100% power while during the period of time for which we are seeking T/S relief the reactor will not exceed 5% power.
The lower power. level of 5% versus 100% would more than offset the consequences of reduced ECCS flow.
In conclusion, operation of Cook 1 with a safety injection pump out of service and a maximum power level of 5% for a brief 'period of time is still bounded by the small LOCA FSAR analysis. In addi tion, the fact that the present analysis has significant margin to 10 CFR 50.46 PCT limits indicates that startup of the plant from this refueling outage is not a safety concern.}}

Latest revision as of 12:54, 22 October 2019

Documents Discussions on Request for License Amend Granting Relief from Requirements of Tech Spec 3.5.2 Re Safety Injection Pump Out of Svc.Safety Evaluation Prepared in Conjunction W/Westinghouse Supports Relief Request
ML17334A425
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 09/07/1982
From: Jurgensen R
AMERICAN ELECTRIC POWER SERVICE CORP.
To: Harold Denton, Varga S
NRC, Office of Nuclear Reactor Regulation
References
AEP:NRC:0739, AEP:NRC:739, NUDOCS 8209130234
Download: ML17334A425 (5)


Text

~ ~

ANEPICAN ELECTR1C PGWER Se> vice Corpo~ etio)s 2 Broadu:ay. Xeu: Pork,.l. }. Ir)00.t (2 /2p .S > 0. 9000 September 7, 1982 AEP:NRC:0739 Donald C. Cook Nuclear Plant Unit No. 1 Docket No. 50-315 License No. DPR-58 REQUEST FOR RELIEF FROM TECHNICAL SPECIFICATION 3.5.2 Mr. Harold R. Denton, Director Of fice of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Mr. Steven A. 'Varga

Dear Mr. Denton:

This letter documents the discussions held with members of your Staff concerning our request for a license amendment granting relief from the requirements of .Technical Specification 3.5.2 .

Each Unit of the Cook Nuclear Plant has two Safety Injection Pumps plus two Centrifugal Charging Pumps and two Residual Heat Removal Pumps.

In preparation for the blackout test performed on August 14, 1982, Unit No. 1's North Safety Injection Pump suffered severe damage. We

",have proceeded to repair the pump expeditiously but have not been able to complete the repairs as of the time of this letter. Unit No. 1 Technical Specification (T/S) No. 3.5.2 requires, among other things, that two Safety Injection (SI) Pumps be operable in Modes 1, 2 and 3.

Unit No. 1 is currently 'completing its refueling outage and the return to Modes 3, 2 and 1 is prevented by the inoperability of the SI pump and the T/S mentioned above. In order to proceed with the low power physics testing, we request a waiver of the requirement to have two SI pumps operable in Modes 2 (reactor thermal power less than or equal to 5%) and 3 for a period of one week beginning at the time the Unit enters Mode 3.

The South SI pump will be demonstrated operable prior to entering Mode

3. All remaining technical specification requirements will be met.

Attachment 1 to this letter contains the safety evaluation prepared by us in conjunction with Westinghouse.

we were to lose the operable 1S Safety The conclusion is that even if K

Injection Pump sufficient margin P

wy,

@5"-&~9'M~ 'a

wr Mr. H. R. Dent . AEP: NRC: 0739 would still exist to the limits specified in 10 CFR 50.46. Thus, this relief is not detrimental to the health and safety of the public.

I We would appreciate the expeditious handling of this request by your Staff.

AEPSC interprets 10 CFR 170.22 as requiring that a Class III Amendment Fee be paid for the change. A check in the amount of $ 4,000 will be transmitted to you in a future letter.h This Technical Specification relief request has been reviewed by the Cook Plant PNSRC. It will be reviewed by AEPSC's NSDRC at the next

~

scheduled meeting.

Due to this letter being written on short notice, it has not been prepared following our standa"d Corporate Procedures for such letters.

We shall, however, review the letter according to our Corporate Procedures and wil'nform you if any modification is required.

Very truly yours,

/emc Attachment cc: John E. Dolan - Columbus R. S. Hunter M. P. Alexich W. G. Smith, Jr. Bridgman R. C. Callen ' ~ ~

G. Charnoff Joe Williams, Jr.

NRC Resident Inspector at Cook Plant - Bridgman

Attachment to AEP:NRC:0739 LOCA Evaluation for D. C. Cook Unit 1 with One Safet In ection Pum Out of Service The purpose of this evaluation is to assess the effect of one safety injection pump out of service for the Cook Unit 1 Nuclear Plant on Loss of Coolant Accident (LOCA) consequences. Presently, the plant is fueled by Exxon Nuclear Company. However, the evaluation provided below is judged to be applicable to the non 'Westinghouse fuel, since there are no known major design differences that would have a significant impact on the LOCA behavior important for this evaluation.

Lar e Break LOCA Safety injection pump flow provides an insignificant proportion of the total ECCS flow during a large break accident, where RCS pressure rapidly drops to near atmospheric. Accumulator and low head safety injection (RHR) flow are important for this accident. Therefore, the loss of a safety injection pump has a negligible effect on large LOCA calculated peak clad temperature.

Small Break LOCA The plant's protection against small LOCAs comes from a two train system including a total of two safety injection pumps and two high head charging pumps. Small LOCA FSAR licensing analyses assume the worst single failure to be loss of a train, leaving one intermediate head SI pump and one charging pump. The small LOCA analysis yields clad temperatures well below 10 CFR 50.46 limits. This analysis assumption bounds the present plant configuration with one safety injection pump out of service and no single failure.

If the worst single fai lure assumption is considered in addition to the

loss of the safety injection pump, and further, the train lost is assumed

'to have the operational safety injection pump, ECCS flow is delivered from only the high head charging pump. The following paragraphs evaluate this scenario.

Reduction of ECCS flow in the range of 600 to 1200 psia has an adverse

--"effect on calculated clad temperature for a range of small LOCA break sizes. The loss of a safety i njecti on pump has the effect of reducing delivered ECCS flow in that important pressure range. Total ECCS flow will be degraded by approximately 56% averaged over this pressure interval.

Established sensitivity studies have indicated that such a degradation results in as much as a 550oF small LOCA PCT increase.

~

0

~

t ~ .

The small break analysis for Cook 1 does not use the latest NRC approved W small LOCA Evaluation Model. The current small break LOCA EM would calculate a PCT of approximately 1200oF, reduced from 1493 F, predicted by the analysis in the FSAR. This new PCT is established from analysis of a substantially equivalent plant (3250 MWt,4 Loop, same SI S design) analyzed in HCAP-8970-P-A, ,"Westinghouse Emergency Core Co'oling System Small 8reak October, 1975 Model", and applies to Cook.

Additionally, credit for conservative assumptions in the small LOCA FSAR analysis can mitigate the PCT penalty. Also, the current small LOCA FSAR analysis is performed at 100% power while during the period of time for which we are seeking T/S relief the reactor will not exceed 5% power.

The lower power. level of 5% versus 100% would more than offset the consequences of reduced ECCS flow.

In conclusion, operation of Cook 1 with a safety injection pump out of service and a maximum power level of 5% for a brief 'period of time is still bounded by the small LOCA FSAR analysis. In addi tion, the fact that the present analysis has significant margin to 10 CFR 50.46 PCT limits indicates that startup of the plant from this refueling outage is not a safety concern.