IR 05000440/2005010: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
Line 1: Line 1:
{{IR-Nav| site = 05000440 | year = 2005 | report number = 010 | url = https://www.nrc.gov/reactors/operating/oversight/reports/perr_2005010.pdf }}
{{Adams
| number = ML060380729
| issue date = 02/07/2006
| title = IR 05000440-05-010; 10/1/2005-12/31/2005; Perry Nuclear Power Plant; Post-Maintenance Testing
| author name = Satorius M A
| author affiliation = NRC/RGN-III/DRP
| addressee name = Pearce W H
| addressee affiliation = FirstEnergy Nuclear Operating Co
| docket = 05000440
| license number = NPF-058
| contact person =
| document report number = IR-05-010
| document type = Inspection Report, Letter
| page count = 40
}}
 
{{IR-Nav| site = 05000440 | year = 2005 | report number = 010 }}
 
=Text=
{{#Wiki_filter:
[[Issue date::February 7, 2006]]
 
Mr. Acting Vice President
 
FirstEnergy Nuclear Operating Company
 
Perry Nuclear Power Plant
 
10 Center Road, A290
 
Perry, OH 44081
 
SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2005010
 
==Dear Mr. Pearce:==
On December 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection
 
findings that were discussed on January 6, 2006, with you and other members of your staff.
 
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed
 
personnel. In addition to the routine NRC inspection and assessment activities, Perry
 
performance is being evaluated quarterly as described in the Assessment Follow-up Letter -
 
Perry Nuclear Power Plant, dated August 12, 2004. Consistent with Inspection Manual Chapter (IMC) 0305, "Operating Reactor Assessment Progr am," plants in the "Multiple/Repetitive Degraded Cornerstone" column of the NRC's Action Matrix are given consideration at each
 
quarterly performance assessment review for (1) declaring plant performance to be unacceptable
 
in accordance with the guidance in IMC 0305; (2) transferring to the IMC 0350, "Oversight of
 
Operating Reactor Facilities in a Shutdown Condi tion with Performance Problems," process; and (3) taking additional regulatory actions, as appropriate. On December 1, 2005, the NRC
 
reviewed Perry operational performance, inspection findings, and performance indicators for the
 
third quarter of 2005. Based on this review, we concluded that Perry is operating safely. We
 
determined that no additional regulatory actions, beyond the already increased inspection
 
activities and management oversight, are currently warranted.
 
Based on the results of this inspection, three findings of very low safety significance, all of which involved violations of NRC requirements, we re identified. However, because of their very low safety significance and because they have been entered into your corrective action program, the NRC is treating these violations as non-cited violations (NCVs) in accordance with
 
Section VI.A.1 of the NRC's Enforcement Policy.
 
W. Pearce-2-
If you contest the subject or severity of these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
 
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
 
Office at the Perry Nuclear Power Plant.
 
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public
 
Document Room or from the Publicly Ava ilable Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,/RA/Mark A. Satorius, Director Division of Reactor Projects Docket No. 50-440 License No. NPF-58
 
===Enclosure:===
Inspection Report 05000440/2005010
 
===w/Attachment:===
Supplemental Informationcc w/encl:G. Leidich, President - FENOC J. Hagan, Chief Operating Officer, FENOC
 
D. Pace, Senior Vice President Engineering and Services, FENOC
 
Director, Site Operations
 
Director, Regulatory Affairs
 
M. Wayland, Director, Maintenance Department
 
Manager, Regulatory Compliance
 
T. Lentz, Director, Performance Improvement
 
J. Shaw, Director, Nuclear Engineering Department
 
D. Jenkins, Attorney, First Energy
 
Public Utilities Commission of Ohio
 
Ohio State Liaison Officer
 
R. Owen, Ohio Department of Health
 
=SUMMARY OF FINDINGS=
IR 05000440/2005010; 10/1/2005-12/31/2005; Perry Nuclear Power Plant; Post-Maintenance
 
Testing This report covers a 3-month period of baseline inspection. The inspection was conducted by the resident and regional inspectors. This inspection identified three Green findings, all of which involved associated non-cited violations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, "Significance
 
Determination Process". Findings for which the Significance Determination Process does not apply may be "Green" or be assigned a severity level after NRC management review. The
 
NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.
 
===NRC-Identified===
and Self-Revealed Findings
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
A finding of very low safety significance and an associated non-cited violation of Technical Specification 5.4, "Procedures," was self-revealed during Division 2 Emergency
 
Diesel Generator (EDG) post-maintenance testing on September 15, 2005, when the engine-driven fuel oil pump was discovered air bound after licensee personnel failed to implement appropriate procedures for the fill and vent of the pump suction and discharge lines following pump maintenance activities. As a result of operating the pump for about 40 minutes without proper fuel oil flow, the engine-driven fuel oil pump required replacement, which extended the Division 2 EDG maintenance outage by about 24 hours and incurred about 15 hours of unnecessary unavailability. As part of their corrective actions, the licensee removed the EDG from service, replaced the engine-driven fuel oil pump, and successfully re-tested the EDG on September 16, 2005. The primary cause of this finding was related to the cross-cutting area of Human Performance since licensee personnel failed to develop an appropriate fill and vent procedure for the engine-driven fuel oil pump.
 
This finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low safety significance because:  (1) it did not represent an actual loss of safety function of a system; (2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time; (3) it did not represent an actual loss of safety function of one or more non-Technical Specification trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours; and (4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event.  (Section 1R19.1)*Green. A finding of very low safety significance and an associated non-cited violation of Technical Specification 5.4, "Procedures," was self-revealed on October 30, 2005, when licensee personnel failed to develop an appropriate procedure for the replacement of the
 
'B' Emergency Closed Cooling (ECC) pump oil bearing reservoir, which resulted in an oil leak and unnecessary pump unavailability. As part of their corrective actions, licensee personnel completed repairs to the pump on November 1, 2005, which included establishing a correct reservoir height and performing post-maintenance testing with satisfactory results. The primary cause of this finding was related to the cross-cutting area of Human Performance because licensee personnel failed to develop appropriate oil reservoir maintenance procedures.
 
This finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low safety significance because:  (1) it did not represent an actual loss of safety function of a system; (2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time; (3) it did not represent an actual loss of safety function of one or more non-Technical Specification trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours; and (4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event.  (Section 1R19.2)*Green. A finding of very low safety significance and an associated non-cited violation of10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," was self-revealed on
 
November 19, 2005, when licensee personnel failed to promptly correct a condition adverse to quality associated with the development of appropriate procedures for oil reservoir replacement, which resulted in an oil leak on the 'A' ECC pump, incurring unnecessary pump unavailability. As part of their corrective actions, licensee personnel completed repairs to the pump on November 29, 2005, which included establishing a correct reservoir height and performing post-maintenance testing with satisfactory results.
 
The primary cause of this finding was related to the cross-cutting area of Problem
 
Identification and Resolution because licensee personnel failed to correct an inadequate oil reservoir maintenance procedure in a timely manner.
 
This finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low safety significance because:  (1) it did not represent an actual loss of safety function of a system; (2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time; (3) it did not represent an actual loss of safety function of one or more non-Technical Specification trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours; and (4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event.  (Section 1R19.3)
 
4
 
===B. Licensee-Identified Violations===
 
Three violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.
 
5
 
=REPORT DETAILS=
 
===Summary of Plant Status===
 
The plant began the inspection period at 100 percent power. On October 8, 2005, operators reduced reactor power to 95 percent to isolate a main condenser train to address a condenser
 
tube leak and returned to 100 percent power later the same day. On October 12, 2005, operators reduced reactor power to 65 percent in order to perform a condenser tube repair and
 
control rod sequence exchange. After several power maneuvers for rod alignment, operators returned the reactor to 100 percent power on October 15, 2005. The plant remained at
 
100 percent power for the remainder of the inspection period with the exception of planned
 
downpowers for routine surveillance testing and rod sequence exchanges.1.REACTOR SAFETY Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity and Emergency Preparedness1R01Adverse Weather Protection (71111.01)
 
====a. Inspection Scope====
The inspectors reviewed the licensee's procedures and preparations for cold weather conditions. The inspectors reviewed winterization procedures, severe weather
 
procedures, and performed general area walkdowns. During walkdowns conducted the
 
week of October 17, 2005, the inspectors toured selected buildings and areas to
 
determine whether the licensee had identified all discrepant conditions such as damaged
 
doors, windows, or vent louvers. The inspectors reviewed documentation to determine
 
whether licensee procedure PTI-GEN-P0026, "Preparations For Winter Operation,"
 
Revision 2, had been completed prior to the onset of cold weather. Additionally, the
 
inspectors observed housekeeping conditions and verified that materials capable of
 
becoming airborne missile hazards during high wind conditions, or impacting snow
 
removal, were appropriately located and restrained. Finally, the inspectors reviewed the
 
licensee's cold weather readiness to determine whether cold weather protection features
 
such as heat tracing and space heaters were monitored and functional.
 
This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.
{{a|1R04}}
==1R04 Equipment Alignment (71111.04)==
 
====a. Inspection Scope====
The inspectors conducted partial walkdowns of the system trains listed below to determine whether the systems were correctly aligned to perform their designed safety 6 function. The inspectors used licensee valve lineup instructions (VLIs) and system drawings during the walkdowns. The walkdowns included selected switch and valve
 
position checks, and verification of electrical power to critical components. Finally, the
 
inspectors evaluated other elements, such as material condition, housekeeping, and
 
component labeling. The documents used for the walkdowns are listed in the attached
 
List of Documents Reviewed. The inspectors reviewed the following systems:*the Control Complex Chilled Water (CCCW) system 'B' while CCCW 'A' was unavailable due to planned maintenance during the week of October 3, 2005; and*the Division 1 Emergency Diesel Generator (EDG) and support systems on November 16, 2005, following completion of a Division 1 maintenance outage.
 
These reviews represented two inspection samples.
 
====b. Findings====
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection (71111.05AQ)==
 
====a. Inspection Scope====
The inspectors walked down the following areas to assess the overall readiness of fire protection equipment and barriers:*Fire Zone 1DG-1A, Unit 1 Division 2 Diesel Generator Building elevation 620'-6" and 646'-6";*Fire Zone 1DG-1C, Unit 1 Division 1 Diesel Generator Building elevation 620'-6" and 646'-6";*Fire Zone 1AB-1A, Unit 1 - Low Pressure Core Spray System;
*the turbine building (all zones); and
*the heater bay (all zones).
 
Emphasis was placed on evaluating the licensee's control of transient combustibles and ignition sources, the material condition of fire protection equipment, and the material
 
condition and operational status of fire barriers used to prevent fire damage or
 
propagation. The inspectors utilized the general guidelines established in licensee
 
procedures Fire Protection Instruction (FPI)-A-A02, "Periodic Fire Inspections,"
 
Revision 3; Perry Administrative Procedure (PAP)-1910, "Fire Protection Program,"
 
Revision 11; and PAP-0204, "Housekeeping/Cleanliness Control Program," Revision 15;
 
as well as basic National Fire Protection Association Codes, to perform the inspection
 
and to determine whether the observed conditions were consistent with procedures and
 
codes.The inspectors observed fire hoses, sprinklers, and portable fire extinguishers to determine whether they were installed at their designated locations, were in satisfactory
 
physical condition, and were unobstructed. The inspectors also evaluated the physical
 
location and condition of fire detection devices. Additionally, passive features such as fire 7 doors, fire dampers, and mechanical and electrical penetration seals were inspected to determine whether they were in good physical condition. The documents listed at the
 
end of this report were used by the inspectors during the assessment of this area.
 
These reviews represented five inspection samples.
 
====b. Findings====
No findings of significance were identified.
{{a|1R07}}
==1R07 Heat Sink (71111.07)==
 
====a. Inspection Scope====
The inspectors reviewed Residual Heat Removal (RHR) 'A' and RHR 'C' heat exchanger performance testing conducted December 1, 2005. The inspectors reviewed the
 
licensee's preliminary test results and reviewed historical trending data to verify that
 
current testing frequency was sufficient to detect degradation of heat exchanger
 
performance.
 
This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.
{{a|1R11}}
==1R11 Licensed Operator Requalification (71111.11).1Annual Operating Test Results==
 
====a. Inspection Scope====
The inspector reviewed the overall pass/fail results of the annual operating examination, which consisted of Job Performance Measure (JPM) and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee. The
 
operating testing was conducted in November and December 2005. The results were
 
compared with the significance determination process in accordance with NRC Manual
 
Chapter 0609, Appendix I, "Operator Requalification Human Performance Significance
 
Determination Process (SDP)."
 
This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.
 
8.2 Quarterly Inspection
 
====a. Inspection Scope====
On November 22, 2005, the resident inspectors observed licensed operator performance in the plant simulator. The inspectors evaluated crew performance in the areas of:*clarity and formality of communication;*ability to take timely action in the safe direction;
*prioritizing, interpreting, and verifying alarms;
*correct use and implementation of procedures, including alarm response procedures;*timely control board operation and manipulation, including high-risk operator actions; and,*group dynamics.
 
The inspectors also reviewed the licensee's evaluation of crew performance to determine whether the training staff had identified performance deficiencies and specified
 
appropriate remedial actions.
 
This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.
{{a|1R12}}
==1R12 Maintenance Effectiveness (71111.12)==
 
====a. Inspection Scope====
The inspectors reviewed the licensee's implementation of the maintenance rule requirements to determine whether component and equipment failures were identified
 
and scoped within the maintenance rule and that select structures, systems, and
 
components (SSCs) were properly categorized and classified as (a)(1) or (a)(2) in
 
accordance with 10 CFR 50.65. The inspectors reviewed station logs, maintenance work
 
orders (WOs), selected surveillance test procedures, and a sample of condition reports (CRs) to determine whether the licensee was identifying issues related to the
 
maintenance rule at an appropriate threshold and that corrective actions were
 
appropriate. Additionally, the inspectors reviewed the licensee's performance criteria to
 
determine whether the criteria adequately monitored equipment performance and to
 
determine whether licensee changes to performance criteria were reflected in the
 
licensee's probabilistic risk assessment. During this inspection period, the inspectors
 
reviewed the following SSCs:*the DC (direct current) electrical system; *the electrical switchyard; and
*the reactor core isolation cooling system.
 
9 These reviews represented three inspection samples.
 
====b. Findings====
No findings of significance were identified.
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)==
 
====a. Inspection Scope====
The inspectors reviewed the licensee's evaluation of plant risk, scheduling, configuration control, and performance of maintenance associated with planned and emergent work
 
activities to determine whether scheduled and emergent work activities were adequately
 
managed in accordance with 10 CFR 50.65(a)(4). In particular, the inspectors reviewed
 
the licensee's program for conducting maintenance risk assessments to determine
 
whether the licensee's planning, risk management tools, and the assessment and
 
management of on-line risk were adequate. The inspectors also reviewed licensee
 
actions to address increased on-line risk when equipment was out of service for
 
maintenance, such as establishing compensatory actions, minimizing the duration of the
 
activity, obtaining appropriate management approval, and informing appropriate plant staff, to determine whether the actions were accomplished when on-line risk was
 
increased due to maintenance on risk-significant SSCs. The following assessments
 
and/or activities were reviewed:*the licensee's management of emergent work activities associated with a high pressure condenser tube leak and planned switchyard activities during the week
 
of October 10, 2005;*the maintenance risk assessment and risk management actions associated with emergent work on the Division 2 EDG governor control switch on
 
October 18, 2005;*the licensee's risk management of work activities associated with the Division 1 EDG extended outage during the weeks of October 31, 2005, and
 
November 7, 2005;*the maintenance risk assessment and risk management actions associated with the replacement of the Division 2 EDG jacket water cooling pump on
 
December 7, 2005; and*the licensee's risk management of work activities associated with planned maintenance of the Emergency Closed Cooling (ECC) 'B' Pump on December 27, 2005.These reviews represented five inspection samples.
 
====b. Findings====
No findings of significance were identified.
 
101R14Operator Performance During Non-Routine Evolutions and Events (71111.14).1Condenser Tube Leak
 
====a. Inspection Scope====
The inspectors reviewed the licensee's response to increasing condensate conductivity on October 7, 2005. The inspectors reviewed the licensee's immediate and supplemental
 
actions to determine whether they were consistent with actions specified in licensee Off-
 
Normal Instruction (ONI)-N61, "Condenser Tube Leak/Organic Intrusion," Revision 9. The
 
inspectors also observed licensee actions associated with leak isolation and repair.
 
This review represented the first of two inspection samples.
 
====b. Findings====
No findings of significance were identified..2Offgas Building Radiation Monitor Alarms
 
====a. Inspection Scope====
The inspectors observed the licensee's response to offgas building radiation monitor alarms during maintenance on the offgas system on December 21, 2005. The inspectors
 
observed the licensee's immediate and supplemental actions to determine whether they
 
were consistent with actions specified in ONI-D17, "High Radiation Levels Within Plant,"
 
Revision 10.
 
This review represented the second of two inspection samples.
 
====b. Findings====
No findings of significance were identified.
{{a|1R15}}
==1R15 Operability Evaluations (71111.15)==
 
====a. Inspection Scope====
The inspectors selected CRs related to potential operability issues for risk-significant components and systems. These CRs were evaluated to determine whether the
 
operability of the components and systems was justified. The inspectors compared the
 
operability and design criteria in the appropriate sections of the Technical Specifications (TS) and Updated Safety Analysis Report (USAR) to the licensee's evaluations, to
 
determine whether the components or system s were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the
 
measures were in place, would function as intended, and were properly controlled.
 
Additionally, the inspectors determined, where appropriate, compliance with bounding 11 limitations associated with the evaluations. The inspectors reviewed the following issues:*the licensee's conclusions regarding the operability of the Division 1 EDG after the identification of a 25 drop-per-minute jacket water leak on October 5, 2005;*the licensee's assessment of the affect of degrading Division 2 EDG jacket water keep-warm pump seal leakage on Division 2 EDG operability on
 
October 25, 2005;*the licensee's justification for an operability determination request after identifying an oil leak associated with the ECC 'B' pump on October 30, 2005; and*the licensee's evaluation of nonconforming conditions associated with the EDG exhaust corridor heat shield during the week of November 7, 2005.
 
These reviews represented four inspection samples.
 
====b. Findings====
No findings of significance were identified.
{{a|1R16}}
==1R16 Operator Workarounds (71111.16)==
 
====a. Inspection Scope====
During the week ending October 15, 2005, the inspectors performed a semiannual review of the cumulative effects of operator workarounds (OWAs). The list of open OWAs was
 
reviewed to identify any potential effect on the functionality of mitigating systems.
 
Inspection activities included, but were not limited to, a review of the cumulative effects of
 
the OWA on the availability and the potential for improper operation of the system, for
 
potential impacts on multiple systems, and on the ability of operators to respond to plant
 
transients or accidents. Additionally, the inspectors conducted a review of recent CRs to
 
ensure that OWA related issues were entered into the corrective action program when
 
required.This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.
{{a|1R19}}
==1R19 Post-Maintenance Testing (71111.19)==
 
====a. Inspection Scope====
The inspectors evaluated the following post-maintenance testing (PMT) activities for risk-significant systems to assess the following (as applicable):  the effect of testing on
 
the plant had been adequately addressed; testing was adequate for the maintenance
 
performed; acceptance criteria were clear and demonstrated operational readiness; test
 
instrumentation was appropriate; tests were performed as written; and equipment was
 
returned to its operational status following testing. The inspectors evaluated the activities 12 against TS, the USAR, 10 CFR 50 requirements, licensee procedures, and various NRC generic communications. In addition, the inspectors reviewed CRs associated with PMTs
 
to determine whether the licensee was identifying problems and entering them in the
 
corrective action program. The specific procedures and CRs reviewed are listed in the
 
attached List of Documents Reviewed. The following post-maintenance activities were
 
reviewed:*testing of the Division 1 EDG following planned maintenance on September 14, 2005;*testing of the CCCW 'A' system following maintenance on October 6, 2005;
*testing of the Division 2 EDG governor control switch following switch replacement on October 18, 2005;*testing of the Division 1 EDG logic control board following replacement on November 9, 2005; and*testing of the ECC 'A' pump following emergent maintenance conducted November 29, 2005.
 
These reviews represented five inspection samples.
 
====b. Findings====
.1Inadequate Fill and Vent Procedure Resulted in Division 1 EDG Unavailability Introduction
:  A finding of very low safety significance (Green) and an associated non-cited violation (NCV) of TS 5.4, "Procedures," was self-revealed during Division 2
 
EDG post-maintenance testing on September 15, 2005, when the engine-driven fuel oil
 
pump was discovered air bound after licensee personnel failed to develop appropriate
 
procedures for the fill and vent of the engine-driven fuel oil pump suction and discharge
 
lines following pump maintenance activities. As a result of operating the pump for about
 
40 minutes without proper fuel oil flow, the engine-driven fuel oil pump required
 
replacement, which extended the Division 2 EDG maintenance outage by about 24 hours
 
and incurred about 15 hours of unnecessary unavailability.
 
Description
:  On September 14, 2005, the licensee commenced a planned Division 2 maintenance outage. Planned maintenance activities included the Division 2 EDG and
 
EDG support systems, including the fuel oil system. Licensee personnel completed EDG
 
maintenance on September 15, 2005, and after restoring EDG support systems, the
 
licensee declared the EDG available. The licensee commenced post-maintenance EDG
 
testing at about 5:45 p.m. During the test, the "FUEL PUMP/OS DRIVE FAILURE" alarm
 
was received shortly after the EDG was started and the EDG was stopped in accordance
 
with the governing alarm response instruction. Subsequently, on September 16, 2005, the EDG was again started at 00:54 a.m. to obtain additional data. The "FUEL PUMP/OS
 
DRIVE FAILURE" alarm was again received and pump discharge pressure was noted to
 
be only about 5 pounds per square inch gauge (psig). The licensee removed the EDG
 
from service, replaced the engine-driven fuel oil pump, and successfully tested the EDG.
 
The EDG was declared available at 6:43 p.m. on September 16, 2005 after successful
 
post-maintenance testing and declared operable later that same day.
 
13 Subsequent licensee review identified that the fill and vent procedure specified in Section 0600, step 2, of WO 200135325, dated September 14, 2005, which was used to
 
restore the fuel oil system, was inadequate since the use of the direct current (DC) fuel oil
 
booster pump to prime the system did not fill piping upstream of the engine-driven fuel oil pump discharge check valves. The inspectors determined that failure to develop
 
appropriate procedures for the fill and vent of the engine-driven fuel oil pump suction and
 
discharge lines was a performance deficiency warranting a significance determination.
 
=====Analysis:=====
The inspectors concluded that the finding was greater than minor in accordance with Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
 
Reports," dated September 30, 2005. The finding was associated with the Mitigating
 
Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to
 
initiating events to prevent undesirable consequences. Specifically, licensee personnel
 
failed to develop an appropriate procedure for the fill and vent of the engine-driven fuel oil
 
pump suction and discharge lines that extended the Division 2 EDG maintenance outage
 
by about 24 hours and incurred about 15 hours of unnecessary Division 2 EDG
 
unavailability. The finding also affected the cross-cutting area of Human Performance
 
since licensee personnel failed to develop an appropriate fill and vent procedure.
 
The inspectors completed a significance determination of this issue using Appendix A,"Determining the Significance of Reactor Inspection Findings for At-Power Situations," of
 
IMC 0609, "Significance Determination Process (SDP)," dated November 22, 2005. The
 
inspectors determined that the issue was of very low safety significance, in accordance
 
with the Phase 1 screening worksheet, because:
: (1) it did not represent an actual loss of
 
safety function of a system;
: (2) it did not represent an actual loss of safety function of a
 
single train for greater than its TS allowed outage time;
: (3) it did not represent an actual
 
loss of safety function of one or more non-TS trains of equipment designated as
 
risk-significant per 10 CFR 50.65 for greater than 24 hours; and
: (4) it did not screen as
 
potentially risk significant due to a seismic, fire, flooding, or severe weather initiating
 
event.Enforcement
:  Technical Specification 5.4, "Procedures," requires, in part, that written procedures be implemented covering applicable procedures recommended by Regulatory
 
Guide 1.33, "Quality Assurance Program Requirements (Operation)," Revision 2, dated
 
February 1978. Regulatory Guide 1.33, Appendix A, paragraph 9a, stated, "Maintenance
 
that can affect the performance of safety-related equipment should be properly
 
preplanned and performed in accordance with written procedures, documented
 
instructions, or drawings appropriate to the ci rcumstances."  Contrary to this requirement, the licensee failed to implement procedures that were appropriate to the circumstances in
 
that the instructions provided in Section 0600, step 2, of WO 200135325, dated
 
September 14, 2005, resulted in an inadequate fill and vent of the Division 2 EDG engine-
 
driven fuel oil pump suction and discharge lines following maintenance. However, because of the very low safety significance of the issue and because the issue has been
 
entered into the licensee's corrective action program (CR 05-06668), the issue is being
 
treated as a non-cited violation (NCV) consistent with Section VI.A.1 of the NRC
 
Enforcement Policy (NCV 05000440/2005010-01).
 
14 As part of their corrective actions, licensee personnel removed the EDG from service, replaced the engine-driven fuel oil pump, and successfully re-tested the EDG on
 
September 16, 2005..2Inappropriate Procedure Implementation Resulted in 'B' ECC Pump Unavailability Introduction
:  A finding of very low safety significance (Green) and an associated NCV of TS 5.4, "Procedures," was self-revealed on October 30, 2005, when licensee personnel
 
failed to develop an appropriate procedure for the replacement of a 'B' Emergency
 
Closed Cooling (ECC) pump oil reservoir, which resulted in an oil leak and incurred
 
unnecessary pump unavailability.
 
Description
:  On September 14, 2005, licensee personnel performed maintenance on the
'B' ECC pump that installed a re-designed Trico oil reservoir on the inboard and outboard
 
pump bearings. Subsequently, licensee operating logs documented oil additions to the
 
'B' ECC pump on September 28, 2005, and October 30, 2005.
 
On October 29, 2005, licensee personnel determined that the pump leaked oil when in operation. Licensee personnel questioned the ability of the pump to perform its design
 
basis function, subsequently declared the pump inoperable, and removed the pump from
 
service for repair. Licensee personnel replaced the pump outboard bearing seal to
 
address the oil leakage. On October 31, 2005, the licensee conducted post-maintenance
 
testing and noted that the pump continued to leak oil. After further investigation, licensee
 
personnel determined that the reservoir replacement maintenance activity had resulted in
 
an incorrect installation height for the pump outboard bearing oil reservoir. This resulted
 
in a higher than required oil level in the pump and led to increased pump temperature and
 
seal leakage. As part of their corrective actions, licensee personnel completed repairs to
 
the pump on November 1, 2005, which included establishing a correct reservoir height
 
and performing post-maintenance testing with satisfactory results.
 
The inspectors reviewed WO 200075252 that was used to replace the 'B' ECC pump bearing oil reservoirs on September 14, 2005.
 
The WO prescribed the use of Preventive Maintenance Instruction (PMI)-0050, "Preventive Maintenance Lubricating Guidelines,"
 
Revision 3, to install the reservoir. Section 5.3.2 of PMI-0050, "Opto-Matic Oiler Bottles (Motors, Pumps, Gear Reducers, ect. [sic])," referenced Attachment 2, "Plastic
 
Opto-Matic Oilers," for guidance. Attachm ent 2 was a copy of the September 1989 Trico manufacturer's instructions for installation of Opto-Matic oilers. Attachment 2, step 8, instructed operators to start the machine after oil reservoir installation and observe
 
whether proper oil level was maintained. If oil was not at the proper level, the instruction
 
returned operators to steps 6 and 7 for additional oil reservoir height adjustments.
 
However, the inspectors noted that Section 5.3.2 of PMI-0050 stated that Attachment 2 "may be referred to for guidance on Opto-matic oiler (oil reservoir) alignment," and, as
 
such, the instructions were optional. Section 5.3.2 only required operators to install the
 
reservoir, add oil, and then run the pump for 10 minutes and note any oil leakage.
 
Section 5.3.2 contained no steps to check for proper oil level after oil was added to the
 
pump or after the pump was run. The inspectors noted that the procedure steps in
 
Section 5.3.2 were inconsistent with the vendor guidance in Attachment 2 to check for 15 proper oil level after oil reservoir installation and pump run to verify that the reservoir height was correct. The licensee's performance of PMI-0050 resulted in an incorrect
 
reservoir installation height at the completion of the maintenance. The licensee's post-
 
maintenance testing failed to detect the flawed condition.
 
The licensee concluded that improper installation of the oil reservoir for the 'B' ECC outboard pump bearing led to an oil level that was about 1/4-inch too high. This resulted
 
in an oil leak from the bearing seal.
 
The inspectors determined that the licensee's failure to implement appropriate procedures for the replacement of the oil reservoir on September 14, 2005, which
 
resulted in pump oil leakage and unavailability when the pump was removed from service for necessary repairs, was a performance deficiency warranting a significance evaluation.
 
=====Analysis:=====
The inspectors concluded that the finding was greater than minor in accordance with Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
 
Reports," dated September 30, 2005. Specifically, the finding was associated with the
 
Mitigating Systems cornerstone attribute of equipment performance and affected the
 
cornerstone objective of ensuring the availability, reliability, and capability of systems that
 
respond to initiating events to prevent undesirable consequences. The improper pump oil
 
reservoir installation resulted in an oil leak and unnecessary pump unavailability. The
 
finding affected the cross-cutting area of Human Performance because licensee
 
personnel failed to develop appropriate procedures for the oil reservoir replacement
 
activity.The inspectors completed a significance determination of this issue using Appendix A,"Determining the Significance of Reactor Inspection Findings for At-Power Situations," of
 
IMC 0609, "Significance Determination Process (SDP)," dated November 22, 2005. The
 
inspectors determined that the finding was of very low safety significance, in accordance
 
with the Phase 1 screening worksheet, because:
: (1) it did not represent an actual loss of
 
safety function of a system;
: (2) it did not represent an actual loss of safety function of a
 
single train for greater than its TS allowed outage time;
: (3) it did not represent an actual
 
loss of safety function of one or more non-TS trains of equipment designated as
 
risk-significant per 10 CFR 50.65 for greater than 24 hours; and
: (4) it did not screen as
 
potentially risk significant due to a seismic, fire, flooding, or severe weather initiating
 
event.Enforcement
:  Technical Specification 5.4, "Procedures," required the implementation of the applicable procedures recommended in Regulatory Guide 1.33, "Quality Assurance
 
Program Requirements (Operation)," Revision 2, dated February 1978. Regulatory Guide
 
1.33 Appendix A, Part 9a, stated, "Maintenance that can affect the performance of safety-
 
related equipment should be properly preplanned and performed in accordance with
 
written procedures, documented instructions, or drawings appropriate to the
 
circumstances."  Contrary to this r equirement, the licensee failed to implement procedures that were appropriate to the circumstances during the replacement of the
 
'B' ECC pump outboard bearing oil reservoir on September 14, 2005, which resulted in
 
an incorrect reservoir installation height and an oil leak that led to unnecessary pump
 
inoperability and unavailability. However, because of the very low safety significance of 16 the issue and because the issue has been entered into the licensee's corrective action program (CR 05-07379), the issue is being treated as a non-cited violation (NCV)
 
consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000440/20050010-02).
 
As part of the licensee's corrective actions, on November 1, 2005, the licensee established a correct oil reservoir height and performed post-maintenance testing with satisfactory results..3Failure to Correct an Identified Procedure Issue Resulted in 'A' ECC Pump Unavailability Introduction
:  A finding of very low safety significance (Green) and an associated NCV of10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," was self-revealed on
 
November 19, 2005, when licensee personnel failed to promptly correct a condition
 
adverse to quality associated with the development of appropriate procedures for oil
 
reservoir replacement, which resulted in an oil leak on the 'A' ECC pump and
 
unnecessary pump unavailability.
 
Description
:  On September 14, 2005, licensee personnel performed maintenance on the
'B' ECC pump that installed a re-designed Trico oil reservoir on the inboard and outboard
 
pump bearings. The pump subsequently leaked oil and was declared inoperable and
 
unavailable. The licensee performed maintenance to replace the pump shaft seal to
 
address the oil leakage. Following this maintenance, the licensee noted that the pump
 
continued to leak oil. On October 31, 2005, the licensee identified that the reservoir
 
replacement maintenance activity had resulted in an incorrect reservoir installation height
 
and that this caused the pump to leak oil. Revision 3 of PMI-0050, "Preventive
 
Maintenance Lubricating Guidelines," was the procedure used to install the reservoir.
 
On November 3, 2005, the licensee performed maintenance on the 'A' ECC pump that installed the revised Trico oil reservoir design. Licensee personnel used the same
 
procedure, PMI-0050, Revision 3, to install the reservoir. The pump leaked oil during
 
post-maintenance testing on November 5, 2005, and the licensee determined that this
 
was the result of an incorrect oil reservoir installation height. The licensee performed an
 
adjustment to the reservoir height and declared the pump operable.
 
Subsequently, the November 19, 2005, operator log entries identified that oil was "being slung from the shaft" of the 'A' ECC pump. On November 20, 2005, operators declared
 
the 'A' ECC pump inoperable and shut it down for maintenance. On pump shutdown, the
 
operator logs identified that the inboard bearing was "spraying a mist of oil" and that the
 
reservoir oil level was "at the bottom of the glass."  The licensee identified that the
 
leakage was due to an incorrect oil reservoir height adjustment on the inboard bearing, performed work to correct the condition, and declared the pump operable later the same
 
day.Subsequently on November 28, 2005, the licensee declared the 'A' ECC pump inoperable due to oil leakage from the outboard bearing. The licensee determined that
 
this was caused by an improper oil reservoir height on the outboard bearing. As part of
 
their corrective actions, licensee personnel completed repairs to the pump on 17 November 29, 2005, which included establishing a correct reservoir height and performing post-maintenance testing with satisfactory results.
 
The inspectors noted that the licensee had also performed work to replace the oil reservoirs on the 'A' Turbine Building Closed Cooling Water (TBCCW) pump, a
 
safety-significant pump. This again produced improper oil reservoir installations. On
 
November 15, 2005, the pump reservoirs were replaced. On November 16, 2005, significant oil leakage was noted from the 'A' TBCCW pump and the operator logs
 
identified that the outboard bearing oil reservoir was empty. Condition Report 05-07633, "TBCC Pump A Failed PMT," dated November 16, 2005, stated that "oil covered the floor
 
in the Turbine Building."  Work was performed to address an improper oil reservoir
 
installation on the pump the same day. Subsequently, on November 19, 2005, the 'A'
 
TBCCW pump was again noted to be leaking oil due to an incorrect reservoir height. The
 
licensee repaired the pump on November 22, 2005, with satisfactory results.
 
In summary, the licensee identified that the performance of the oil reservoir replacement maintenance procedure in PMI-0050, Revision 3, resulted in incorrect oil reservoir
 
installations on the 'B' ECC pump. The licensee then subsequently performed the same
 
procedure on other equipment and caused degraded conditions on the 'A' ECC and
 
'A' TBCCW pumps. Additionally, initial post-maintenance testing for both the 'A' ECC
 
and the 'A' TBCCW pumps identified that the maintenance had resulted in improper
 
reservoir installation height. This provided an additional opportunity to address the
 
appropriateness of the reservoir maintenance procedure prior to returning the equipment
 
to service. Therefore, the inspectors determined that reasonable opportunities existed to
 
address the reservoir maintenance issues before performing work on additional
 
safety-related or safety-significant system s, and before returning equipment to service with a degraded condition. The inspectors determined that the failure to promptly correct
 
the deficiencies associated with the reservoir maintenance procedures was a
 
performance deficiency warranting a significance evaluation.
 
=====Analysis:=====
The inspectors concluded that the finding was greater than minor in accordance with Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
 
Reports," dated September 30, 2005. Specifically, the finding was associated with the
 
Mitigating Systems cornerstone attribute of equipment performance and affected the
 
cornerstone objective of ensuring the availability, reliability, and capability of systems that
 
respond to initiating events to prevent undesirable consequences. The failure to promptly
 
correct deficiencies in the reservoir maintenance procedure led to additional safety
 
system degradation and unavailability. The finding affected the cross-cutting area of
 
Problem Identification and Resolution because licensee personnel failed to promptly
 
correct the deficiencies associated with the reservoir maintenance procedure in a timely
 
manner, which resulted in additional incorrect reservoir installations.
 
The inspectors completed a significance determination of this issue using Appendix A,"Determining the Significance of Reactor Inspection Findings for At-Power Situations," of
 
IMC 0609, "Significance Determination Process (SDP)," dated November 22, 2005. The
 
inspectors determined that the issue was of very low safety significance, in accordance
 
with the Phase 1 screening worksheet, because:
: (1) it did not represent an actual loss of
 
safety function of a system;
: (2) it did not represent an actual loss of safety function of a 18 single train for greater than its TS allowed outage time;
: (3) it did not represent an actual loss of safety function of one or more non-TS trains of equipment designated as
 
risk-significant per 10 CFR 50.65 for greater than 24 hours; and
: (4) it did not screen as
 
potentially risk significant due to a seismic, fire, flooding, or severe weather initiating
 
event.Enforcement:  10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly
 
identified and corrected. Contrary to this requirement, on October 31, 2005, during
 
maintenance on the 'B' ECC pump, licensee personnel identified that oil reservoir
 
maintenance procedure PMI-0050, "Preventive Maintenance Lubricating Guidelines,"
 
Revision 3, was inadequate in that it resulted in an incorrect reservoir installation height.
 
The licensee failed to correct the procedure in a timely manner and, as a result, on
 
November 3, 2005, applied the same procedure to the 'A' ECC pump, resulting in
 
unnecessary pump inoperability and unavailability. However, because of the very low
 
safety significance of the issue and because the issue has been entered into the
 
licensee's corrective action program (CR 05-07688), the issue is being treated as an NCV
 
consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000440/20050010-03).
 
As part of their corrective actions, licensee personnel completed repairs to the pump on November 29, 2005, which included establishing a correct reservoir height and
 
performing post-maintenance testing with satisfactory results.
{{a|1R22}}
==1R22 Surveillance Testing (71111.22)==
 
====a. Inspection Scope====
The inspectors observed surveillance testing or reviewed test data for risk-significant systems or components to assess compliance with TS; 10 CFR 50, Appendix B; and
 
licensee procedure requirements. The testing was also evaluated for consistency with
 
the USAR. The inspectors verified that the testing demonstrated that the systems were
 
ready to perform their intended safety functions. The inspectors determined whether test
 
control was properly coordinated with the control room and performed in the sequence
 
specified in the surveillance instruction (SVI), and if test equipment was properly
 
calibrated and installed to support the surveillance tests. The procedures reviewed are
 
listed in the attached List of Documents Reviewed. The surveillance activities assessed
 
were:*main steam isolation valve and logic functional testing conducted October 22, 2005;*CCCW 'B' pump and valve testing conducted October 28, 2005;
*remote shutdown panel control operability test for RHR 'A,' ESW 'A,' and ECC 'A' conducted during the week of October 31, 2005;*high pressure core spray (HPCS) pump and valve operability test on November 15, 2005;*the Division 1 EDG monthly surveillance conducted December 28, 2005.
 
19 These reviews represented five inspection samples.
 
====b. Findings====
No findings of significance were identified.
{{a|1R23}}
==1R23 Temporary Plant Modifications (71111.23)==
 
====a. Inspection Scope====
The inspectors reviewed the documentation for a contingency temporary configuration change associated with installation of an alternate air charging system for the Division 2
 
EDG. The inspectors reviewed the temporary configuration change and the
 
10 CFR 50.59 screening and evaluation information against the design basis, the USAR
 
and the TS as applicable. The inspectors walked down the locations of all staged
 
equipment associated with this modification to determine whether plant safety systems were adversely impacted.
 
This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.1EP2Alert and Notification System Testing (71114.02)
 
====a. Inspection Scope====
The inspectors discussed with Emergency Preparedness (EP) staff the operation, maintenance, and periodic testing of the Alert and Notification System (ANS) in the Perry
 
Nuclear Power Plant's plume pathway Emergency Planning Zone to determine whether
 
the ANS equipment was adequately maintained and tested in accordance with
 
Emergency Plan commitments and procedures. The inspectors reviewed records of
 
2004 and 2005 preventative, non-scheduled maintenance activities and weekly
 
operability test results.
 
These activities represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.1EP3Emergency Response Organization Augmentation Testing (71114.03)
 
====a. Inspection Scope====
20 The inspectors reviewed and discussed with plant EP staff the emergency plan commitments, emergency implementing procedures (EPI), and other instructions that
 
addressed the primary and alternate methods of initiating an Emergency Response
 
Organization (ERO) activation to augment the on-shift ERO, as well as the provisions for
 
maintaining the plant's ERO call-out roster and emergency telephone directory. The
 
inspectors also reviewed reports and a sample of corrective action program records of
 
unannounced off-hour augmentation tests, which were conducted in 2004 and 2005, to
 
determine the adequacy of the drills' critiques and associated corrective actions. The
 
inspectors also reviewed the EP training records of a sample of 17 Perry Power Plant
 
ERO personnel, who were assigned to key and support positions, to determine whether
 
they were currently trained for their assigned ERO positions.
 
These activities represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.1EP4Emergency Action Level and Emergency Plan Changes (71114.04)
 
====a. Inspection Scope====
The inspectors performed a screening review of portions of Revisions 22 and 23 of the Perry Nuclear Plant Emergency Plan to determine whether the changes made in these
 
revisions decreased the effectiveness of the licensee's emergency planning. This
 
screening review did not constitute an approval of the changes and, as such, the changes
 
are subject to future NRC inspection to ensure that the emergency plan continues to
 
meet NRC regulations.
 
These activities represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)
 
====a. Inspection Scope====
The inspectors reviewed Nuclear Oversight staff's 2004 and 2005 reviews of the licensee's EP program to verify that these independent assessments met the
 
requirements of 10 CFR 50.54(t). The inspectors reviewed a sample of CR records
 
associated with those reviews to determine whether Nuclear Oversight concerns were
 
being addressed. The inspectors also reviewed critique reports and samples of CR
 
records associated with the 2004 biennial exercise in order to verify that the licensee
 
fulfilled its annual drill commitments and to evaluate the licensee's efforts to adequately
 
identify, track, and resolve concerns identified during these activities.
 
21 These activities represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.1EP6Drill Evaluation (71114.06)
 
====a. Inspection Scope====
The inspectors observed activities in the simulator control room, the technical support center, the emergency operations facility, and operations support center during an
 
emergency preparedness drill conducted on October 11, 2005. The inspection focused
 
on the ability of the licensee to appropriately classify emergency conditions, complete
 
timely notifications, and implement appropriate protective action recommendations in
 
accordance with approved procedures.
 
This review represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.4.
 
==OTHER ACTIVITIES==
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
 
====a. Inspection Scope====
===Cornerstone:===
Emergency Preparedness The inspectors reviewed the licensee's records associated with the three EP performance indicators (PIs) listed below. The inspectors verified that the licensee accurately reported
 
these indicators in accordance with relevant procedures and Nuclear Energy Institute
 
guidance endorsed by the NRC. Specifically, the inspectors reviewed licensee records
 
associated with PI data reported to the NRC for the period July 2004 through September
 
2005. Reviewed records included procedural guidance on assessing opportunities for the
 
three PIs; assessments of PI opportunities during pre-designated Control Room
 
Simulator training sessions, the 2004 biennial exercise, and other drills; revisions of the
 
roster of personnel assigned to key ERO positions; and results of periodic Alert and
 
Notification System (ANS) operability tests. The following PIs were reviewed:*ANS;*ERO Drill Participation; and
*Drill and Exercise Performance.
 
These activities represented three inspection samples.
 
====b. Findings====
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152).1Routine Review of Identification and Resolution of Problems
 
====a. Inspection Scope====
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine whether they
 
were being entered into the licensee's corrective action program at an appropriate
 
threshold, that adequate attention was being given to timely corrective actions, and that
 
adverse trends were identified and addressed.
 
This is not an inspection sample.
 
====b. Findings====
No findings of significance were identified..2Annual Sample Review - 10 CFR 50.59 Review
 
====a. Inspection Scope====
As discussed in NRC Inspection Report 05000440/2005003, dated July 8, 2005, a finding of very low safety significance and an associated NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," was NRC-identified when licensee personnel failed to
 
adequately address a nonconforming condition in the design of the EDGs. This condition
 
made the EDGs vulnerable to damage in response to a loss of offsite power (LOOP)
 
signal under certain scenarios. The licensee contested this violation by letter dated
 
August 8, 2005, with one of the reasons given that a LOOP start was not an "emergency"
 
start. During NRC followup of the contested violation, the NRC requested the safety
 
evaluation associated with PNPP [Perry Nuclear Power Plant] Change Request 88-127, dated December 17, 1988, which revised the wording for Final Safety Analysis Report (FSAR) Section 8.3.1.1.3.2.b.7(e) from "emergency start signal" to "LOCA [Loss of
 
Coolant Accident] start signal."  Following that request, licensee personnel were unable to
 
locate either the change request or the safety evaluation for this change and generated
 
CR 05-06193 "USAR Change Request and 10 CFR 50.59 Review Paperwork Could Not
 
Be Located," to document this issue. By letter dated September 7, 2005, the NRC
 
disputed the licensee's denial of NCV 05000440/2005003-14 because the NRC found
 
that a LOOP signal was, in fact, an emergency start signal, as was stated in numerous
 
other FSAR/Updated Safety Analysis Report (USAR) sections.
 
After further review, the licensee located Change Request 88-127 and Safety Evaluation 88-179; the 10 CFR 50.59 review package referenced in CR 05-06193.
 
23 On September 14, 2005, the licensee initiated CR 05-06622, "NRC Denial of Disputed NCV 2005003-14 (EDG Design Basis Issue)," to address the design changes to be
 
implemented to address the start of the EDGs during the first 2 minutes following an
 
engine shutdown. In CR 05-06622, the licensee noted that Change Request 88-127 had
 
been evaluated as an administrative change rather than a technical change; therefore, the 10 CFR 50.59 review may have been inadequate. The licensee initiated
 
CR 05-07104, "Inadequate 10 CFR 50.59 Evaluation of USAR Change," on
 
October 12, 2005, to document the issue. CR 05-07104 was closed to the investigation
 
and corrective actions associated with CR 05-06622, since this CR would direct any
 
necessary changes to bring the EDG starting signal back into compliance with the USAR.
 
The licensee initiated an action to prepare an engineering change to correct the EDGs
 
failure to start from an under-voltage, or a degraded voltage signal from an associated
 
bus, during the 2 minutes after an engine shutdown. In CR 05-06622, the licensee
 
completed a technical review of Safety Evaluation 88-179, which found the evaluation to
 
be correct.
 
The inspectors selected CR 05-06193, "USAR Change Request and 10 CFR 50.59 Review Paperwork Could Not Be Located," dated August 23, 2005, for detailed review.
 
This review represented one inspection sample.
 
====b. Findings and Observations====
No findings of significance were identified.
 
The inspectors reviewed the licensee's 10 CFR 50.59 evaluation, including Change Request 88-127 and Safety Evaluation 88-179, and determined that since the USAR
 
section being revised was strictly associated with the response of an EDG to a LOCA
 
signal, the change was appropriate. However, the inspectors also noted, as was
 
identified in other sections of the USAR, the EDGs are required to automatically start
 
upon receipt of a signal other than a LOCA signal, such as an under-voltage signal, or a
 
degraded voltage signal from the EDG's associated bus.
 
Therefore, the inspectors concluded that although the licensee's 10 CFR 50.59 evaluation was adequate and the licensee's evaluations in CR 05-6622 were correct
 
when limited to USAR Section 8.3.1.1.3.2.b.7; the overall starting requirements for the
 
EDGs were more extensive, as was reflected in other sections of the USAR..3Semi-Annual Trend Review  a.The inspectors reviewed monthly performance reports, self-assessments, quality assurance assessment reports, performance im provement initiatives and CRs to identify any trends that had not been adequately evaluated or addressed by proposed corrective
 
actions.These reviews did not constitute an inspection sample. b .Findings 24  No findings of significance were identified..4Problem Identification and Resolution Biennial Review This review was completed by reference during the Perry IP 95003 supplemental inspection conducted from January through May 2005 and documented in NRC
 
Inspection Report 05000440/2005003.4OA3Event Followup (71153).1(Closed) Licensee Event Report (LER) 2005-03-00
:  Lack of Suction Path Causes High Pressure Core Spray to be Inoperable. A discussion of this event, and an associated
 
licensee-identified NCV, is contained in Section
{{a|4OA7}}
==4OA7 of this report.==
 
This review represented the first of two samples for this inspection procedure..2Reportable Events and Configuration Control Issues During Scheduled Division 1 Maintenance Outage On November 3 and November 4, 2005, the licensee responded to several emergent configuration control issues associated with plant safety systems. The issues included:
: (1) a tagout that inadvertently rendered a nuclear closed cooling containment isolation
 
valve as well as the 'A' annulus exhaust gas treatment system inoperable;
: (2) a breaker found open that affected the operability of the 'A' emergency service water remote
 
shutdown system; and
: (3) a breaker found open associated with the 'A' standby liquid
 
control system. The inspectors observed the licensee response and reviewed the
 
licensee's actions to determine compliance with licensee procedures, TS, and the
 
reporting requirements of 10 CFR 50.72. Two violations of very low safety significance (Green) were identified by the licensee and are documented in Section
{{a|4OA7}}
==4OA7 of this==
 
report.This review represented the second of two inspection samples for this inspection procedure.4OA5Other (71114.03)
Use of Adjustment Factors to Meet ERO Staffing Timeliness Goals (URI 05000440/2005003)
The inspectors discussed with licensee staff the Perry IP 95003 supplemental inspection report, which identified an unresolved item (URI) regarding the use of adjustment factors
 
to meet ERO staffing timeliness goals. The inspectors advised the licensee that this
 
issue will continue to be evaluated during the follow-up to the IP 95003 Supplemental
 
Inspection early in 2006.
 
This is not an inspection sample.4OA6Meetings 25.1Exit Meeting On January 6, 2006, the resident inspectors presented the inspection results to Mr. W. Pearce, Acting Vice President, and other members of his staff who acknowledged
 
the findings.
 
The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified..2Interim Exit Meetings Exit meetings were conducted for:
*Operator Requalification Program Examination Result Review with Mr. W. O'Malley on December 16, 2005 by telephone.*Emergency Preparedness inspection with Messrs. W. Pearce, R. Anderson, F. von Ahn, and other members of licensee management on December 9, 2005.
 
A telephone exit was held on December 16, 2005, with Messrs. V. Higaki, Fleet
 
Operations Manager; and L. Burgwald, Emergency Preparedness Senior
 
Specialist.4OA7Licensee-Identified Violations The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of
 
the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.
 
===Cornerstone:===
Barrier Integrity
*Technical Specification 5.4, "Procedures," required the implementation of the applicable procedures recommended in Regulatory Guide 1.33, "Quality
 
Assurance Program Requirements (Operation)," Revision 2, dated February 1978.
 
Regulatory Guide 1.33, Appendix A, Part 1.c, recommended procedures for
 
equipment control. Contrary to this requirement, on November 3, 2005, licensee
 
personnel failed to control the impact of a clearance that removed logic fuses
 
associated with Group 2A containment isolation valves and failed to enter
 
numerous required TS action statements. The licensee entered the issue into
 
their corrective action program as CR 05-07442. The inspectors determined that
 
the issue was of very low safety significance because it:
: (1) did not represent a
 
degradation of the barrier function of the control room against smoke or toxic
 
atmosphere; and
: (2) did not represent an actual open pathway in the physical
 
integrity or reactor containment, or involve an actual reduction in defense-in-depth
 
for the atmospheric pressure control or hydrogen control functions of the reactor
 
containment.
 
===Cornerstone:===
Mitigating Systems 26Technical Specification 5.4, "Procedures," required the implementation of the applicable procedures recommended in Regulatory Guide 1.33, "Quality
 
Assurance Program Requirements (Operation)," Revision 2, dated February 1978.
 
Regulatory Guide 1.33, Appendix A, Paragraph 4, required procedures for the
 
operation of safety-related boiling water reactor systems. Similarly, Paragraph
 
8.b.(2)(j) required specific procedures for ECC system surveillance tests.
 
Contrary to this requirement, on September 20, 2005, licensee personnel
 
identified that SVI-E22-T2001, "HPCS [High Pressure Core Spray] Pump and
 
Valve Operability Test," Revision 17, prescribed steps that simultaneously closed
 
both HPCS suction valves without HPCS being declared inoperable. The licensee
 
subsequently identified that SOI-E22A, "High Pressure Core Spray System,"
 
Revision 13, prescribed steps in the HPCS system operating instruction for
 
swapping the suction source from the suppression pool to the condensate storage
 
tank that resulted in the same condition. The licensee determined that an
 
inadvertent manual start or non-time-del ayed automatic start of the HPCS pump with both suction valves closed could pr event the HPCS system from performing its intended function or could result in equipment damage. Licensee log reviews
 
estimated that the system was in this vulnerable configuration (no aligned suction
 
source) for about 14 hours over the past 3 years. Licensee personnel determined
 
that the primary cause of the event was a personnel knowledge deficiency and
 
inadequate procedural guidance.
 
The inspectors determined the issue was more than minor in that the unrecognized system inoperability was related to the maintenance risk
 
assessment and risk management issues specified in Appendix B, "Issue
 
Screening," of IMC 0612, "Power Reactor Inspection Reports," dated
 
September 30, 2005. The inspectors performed a Phase 1 review in accordance
 
with Appendix A, "Determining the Significance of Reactor Inspection Findings for
 
At-Power Situations," of IMC 0609, "Significance Determination Process (SDP),"
 
dated November 22, 2005. The inspectors determined that a Phase 2 review was
 
required because the finding represented a loss of system safety function. The
 
inspectors conducted a Phase 2 review and determined that a Phase 3 review
 
was required. The Region III Senior Reactor Analyst performed a Phase 3
 
evaluation of the finding assuming that the HPCS pump was unavailable for
 
14 hours. The Perry Simplified Plant Analysis Risk (SPAR) analysis, Revision 3.21, was used to perform the evaluation. The result was a change in
 
core damage frequency (CDF) significantly less than 1E-6. The dominant
 
sequence involved a loss of offsite power, failure of the emergency power system, failure of the HPCS system, and the failure to recover offsite power. As such, the
 
finding was determined to be of very low safety significance. The licensee
 
entered this finding into their corrective action program as CR 05-6751.Technical Specification 5.4, "Procedures," required the implementation of the
 
applicable procedures recommended in Regulatory Guide 1.33, "Quality
 
Assurance Program Requirements (Operation)," Revision 2, dated February 1978.
 
Regulatory Guide 1.33, Appendix A, Part 1.c., recommended procedures for
 
equipment control. Contrary to this requirement, on November 3, 2005, licensee
 
personnel identified that a breaker affecting the ESW 'A' remote shutdown 27 ventilation system was incorrectly left in the open position. The licensee determined that a clearance restoration incorrectly restored the breaker to the "off"
 
position on March 27, 2005. This breaker affected the back-up control power
 
required to be available for the 'A' ventilation train. For a control room fire hot
 
short scenario, if power had been selected to the back-up source, the ESW
 
ventilation system would have shut down and the ESW pumphouse could have exceeded its maximum operating temperature. The licensee restored the breaker
 
on November 3, 2005, and entered the issue into their corrective action program
 
as CR 05-07435. The inspectors used Appendix F, "Fire Protection Significance
 
Determination Process," dated February 28, 2005 of IMC 0609, "Significance
 
Determination Process," dated November 22, 2005, to assess the significance.
 
The inspectors determined that the issue was of very low safety significance
 
because it was categorized as a "Cold Shutdown" finding per Step 1.1 and was
 
bounded by Step 1.3 in that it only affected the ability to reach and maintain cold
 
shutdown conditions.
 
ATTACHMENT: 
 
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
 
===Licensee personnel===
: [[contact::W. Pearce]], Acting Vice President
: [[contact::F. von Ahn]], General Manager, Nuclear Power Plant Department
: [[contact::R. Anderson]], Vice President, Operations
: [[contact::N. Bonner]], Manager, Perry Oversight
: [[contact::F. Cayia]], Director, Performance Improvement
: [[contact::K. Cimorelli]], Manager, Work Management
: [[contact::V. Higaki]], Manager, Fleet Operations
: [[contact::J. Lausberg]], Manager, Regulatory Compliance
: [[contact::T. Lentz]], Director, Performance Improvement Initiative
: [[contact::J. Messina]], Manager, Operations
: [[contact::J. Shaw]], Director, Engineering
: [[contact::M. Wayland]], Maintenance Manager
 
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
 
===Opened and Closed===
05000440/2005010-01NCVInadequate Fuel Oil Pump Procedures Resulted in Division 2
EDG Unavailability (Section 1R19.1)05000440/2005010-02NCVInadequate Oil Reservoir Maintenance Procedure
Implementation for ECC 'B' Pump Resulted In Oil Leak
(Section 1R19.2)05000440/2005010-03NCVFailure to Correct an Oil Reservoir Maintenance Procedure
Issue Resulted In ECC 'A' Oil Leak (Section 1R19.3)
Closed2005-03-00LERLack of Suction Path Causes High Pressure Core Spray to
be Inoperable (Section 4OA3)
 
===Discussed===
05000440/2005003-01URIUse of Adjustment Factors to Meet ERO Staffing
Timeliness Goals (Section 4OA5)
 
==LIST OF DOCUMENTS REVIEWED==
The following is a list of documents reviewed during the inspection.
: Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety but rather that
 
selected sections of portions of the documents were evaluated as part of the overall inspection
 
effort.
: Inclusion of a document on this list does not imply NRC acceptance of the document or
 
any part of it, unless this is stated in the body of the inspection report.
 
==Section 1R01: Adverse Weather Protection==
: IOI-15; Seasonal Variations; Revision 7
: ONI-R36-2; Extreme Cold Weather; Revision 1
: PTI-GEN-P0026; Preparations for Winter Operation; Revision 2
: PTI-GEN-P0027; Cold Weather Support System Startup; Revision 7
: PTI-GEN-P0027; Cold Weather Support System Startup; Revision 8
: SOI-R36; Heat Trace and Freeze Protection System; Revision 6
: SOI-P45/49; Emergency Service Water and Screen Wash Systems; Revision 11
 
==Section 1R04: Equipment Alignment==
: VLI-P47; Control Complex Chilled Water System; Revision 6
: SOI-P47; Control Complex Chilled Water System; Revision 13
: VLI-R47; Division 1 and 2 Diesel Generator Lube Oil; Revision 5
: VLI-R44; Division 1 and 2 Diesel Generator Starting Air System (Unit 1); Revision 4
: VLI-R48; Division 1 and 2 Diesel Generator Exhaust, Intake and Crankcase Systems; Revision 6
: VLI-R46; Division 1 and 2 Diesel Generator Jacket Water Systems (Unit 1); Revision 3
: VLI-R45; Division 1 and 2 Diesel Generator Fuel Oil System (Unit 1); Revision 4
: WO 200161353; Level Element for Division 1 EDG Fuel Oil Storage Tank; dated July 21, 2005
 
==Section 1R05: Fire Protection==
: FPI-1DG; Diesel Generator Building; Revision 4
: FPI-TB; Turbine Building; Revision 2
: FPI-HB; Heater Bay; Revision 1
: FPI-1AB; Auxiliary Building Unit 1; Revision 2
 
==Section 1R07: Heat Sink==
: WO 200150844; RHR Exchangers 'A' And 'C' Performance Testing; dated December 1, 2005
: PTI-E12-P0002; RHR Heat Exchanger 'A' and 'C' Performance Testing Trend Chart; dated
: December 20, 2000
 
==Section 1R12: Maintenance Effectiveness==
: CR 05-06331; Incorrect Functional Location in Order; dated August 30, 2005
: CR 05-05822; RFA [Request for Assistance] - As Found Contact Resistance High; dated
: August 3, 2005
: CR 05-05697; WO Given to Operations for Restoration Prior to Post Maint Requirements Completion; dated July 28, 2005
: CR 05-05560; PCR [Procedure Change Request] - Deficiency
: ONI-R42-5; dated July 23, 2005
: CR 05-04861; Bus
: ED-2-C Ground Detection; dated June 16, 2005
: CR 05-04567; Category "A" Limits Not Met on Unit 1 Division 2; dated May 31, 2005
: CR 05-02416;
: ED-1-B Ground Alarm in Control Room; dated March 16, 2005
: CR 05-01350; Loss of D1B07; dated February 23, 2005
: CR 05-05622; Evaluate NRC Information Notice 2005-21 - Switchyard Maintenance
: Issues/Effects; dated July 26, 2005
: CR 05-05500; Fleet Focused Self-Assessment On Switchyard, Transformer & Grid Reliability;
 
dated July 21, 2005
: CR 05-03354; OE19195 - Switchyard Disconnect Switches Indicate Higher Than Normal
: Temperature; dated April 13, 2005
: CR 05-02232; Inadequate Communication of Changes in Transmission Switchyard Work; dated
: March 14, 2005
: CR 05-02046; PII [Performance Improvement Init iative] B Work Management Action: Improve Program Interface with Switchyard Work; dated March 10, 2005
: CR 04-02014; RCIC Turbine Exhaust Pressure Runs High; dated April 19, 2004
: CR 04-02384; Leakage Identified Associated with RCIC System; dated May 11, 2004
: CR 04-03680; 1E51F0022 Failed to Meet its Stroke Time Close; dated July 15, 2004
: CR 04-03721; RCIC Governor Valve Stuck During
: SVI-E51T2001; dated July 17, 2004
: CR 04-03789; Reactor Core Isolation Cooling Periodic Maintenance/Test Scope/Frequency
: Review; dated July 20, 2004
: CR 04-05756; PII Latent Issues Review Identified 1E51F015 Not Tested or Maintained; dated
: November 2, 2004
: CR 04-05790; PII Latent Issues RCIC Review - USAR Table 6.2-32 Update; dated
: November 4, 2004
: CR 04-05975; PII LIR Calculation
: ECA-068 Assumption Not Justified; dated November 16, 2004
: CR 04-06169; RCIC System Walkdown Deficiency; dated November 10, 2004
: CR 04-06252; Planned Performance of Testing on Protected Equipment (RCIC) During Div 1
: Outage; dated November 29, 2004
 
==Section 1R13: ==
: Maintenance Risk Assessments and Emergent Work Control On-Line Probabilistic Safety Assessment; Week 11, Period 2; Revision 2
: PAP [Perry Administrative Procedure] -1924; Risk-Informed Safety Assessment and Risk
: Management; Revision 4
: Main Condenser Leak Downpower Schedule; dated October 12, 2005
: On-Line Probabilistic Safety Assessment; Week 12, Period 2; Revision 1
: Perry Work Implementation Schedule; Week 7, Period 3
 
==Section 1R14: Operator Performance During Non-routine Evolutions and Events==
: ONI [Off-Normal Instruction] -N61; Condenser Tube Leak/Organic Intrusion; Revision 9
: REC-0104; Chemistry Specifications; Revision 15
: SOI [System Operating Instruction] -N71; Circulating Water/Condenser Mechanical Cleaning
: System; Revision 11
: 5
 
==Section 1R15: Operability Evaluations==
: CR 05-07098; Division 1 Diesel Left Bank 4 Cylinder Has Jacket Water Leakage; dated October 5, 2005
: CR 01-0531; Diesel Generator Jacket Water Leakage; dated February 15, 2001
: Calculation R46T03; NonSafety-Related Setpoint Tolerance Calculation for 1R46N0062A(B)
: Diesel Jacket Water Stand Pipe Water Level; Revision 3
: CR 04-02772; Division 2 Jacket Water Keepwarm Pump Leak; dated May 27, 2004
: CR 05-07314; Sensitivity and Timely Response on Lower Level Issues Associated with Safety-
: Related Equipment; dated October 26, 2005
: CR 05-07467; Diesel Hallway Insulation Unistrut Loose Bolt; dated November 6, 2005
: CR 05-07340; 3 Loose Fasteners in DG Exhaust Ha llway Near Construction Opening; dated October 27, 2005
 
==Section 1R16: Operator Workarounds==
: CR 05-05079; Benchmarking Trip to Monticello Nuclear Power Plant Report; dated June 29, 2005
: CR 05-05605; M&C 14, Work Arounds Policy, is Not Effective; dated July 25, 2005
: CR 05-05867; 2
nd Quarter Assessment of Control Room Deficiencies, Work Arounds, and Burdens; dated August 8, 2005
: CR 05-06962; Operator Workarounds Dropped at T+10 Due to Uncompleted ECP; dated
: September 30, 2005
: List of Operator Burdens; dated October 4, 2005
 
==Section 1R19: Post-Maintenance Testing==
: WO 200138847; Calibration Check for OM26N0711A; dated October 6, 2005
: WO 200097190; Control Room Emergency Recirculation A; dated October 5, 2005
: WO 200138846; Calibration Check for OM26N0708A; dated October 6, 2005
: WO 200134210; Control Room Emergency Recirculation A PMT; dated October 6, 2005
: FTI-F0036; Post-Maintenance Test Manual; Revision 3
: WO 200173745; Replace S8 on 1H13P877; dated October 18, 2005
: PTI-R43-P0006-A; Division 1 Diesel Generator Pneumatic Logic Board Functional Check;
: Revision 5
: CR 05-07511; Failure of a Newly Installed Pneumatic Logic Board for Division 1 Diesel
: Generator; dated November 8, 2005
: CR 05-07505; Procedure Errors in
: PTI-R43P0006A; dated November 9, 2005
: PMI-0050; Preventative Maintenance Lubricating Guidelines; Revision 3
: WO 200188113; Emergency Closed Cooling Pump Outboard Bearing Oil Bubbler; dated
: November 29, 2005
: CR 05-07371; ECC Pump 1P42C0001B Outboard Pump Bearing Oil Leak; dated
: October 29, 2005
: CR 05-07383; Oil Leak on Outboard Oil Seal; dated October 31, 2005
: CR 05-07379; Failed PMT for ECC B; dated October 31, 2005
: CR 05-07404; Operability Determination Extension Requested; dated October 31, 2005
: CR 05-07685; Emergency Closed Cooling Pump A Inboard Bearing Bubbler Adjustment; dated
: November 19, 2005
: WO 200187088; ECC Pump A Bubbler Rework; dated November 28, 2005
: WO 200146833; ECC Pump A Bubbler Replacement; dated November 5, 2005
: WO 200075252; ECC Pump B Maintenance and Bubbler Replacement; dated
: September 14, 2005
: CR 05-07633; TBCC Pump A Failed PMT [Post Maintenance Test]; dated November 16, 2005
: CR 05-07683; TBCCW Pump A - Failed PMT/Repeat Maintenance; dated November 19, 2005
 
==Section 1R22: Surveillance Testing==
: SVI-C71-T0039; MSIV [Main Steam Isolation Valve] Closure Channel Functional; Revision 6
: SVI-P47-T2001-B; Control Complex Chilled Water B Pump and Valve Operability Test;
: Revision 3
: SVI-C61-T1201; Remote Shutdown Panel 1C61-P001 Control Operability Test RHR A, ESW A, And ECC A; Revisions 1, 2, 3, and 4
: SVI-E22-T2001; HPCS Pump and Valve Operability Test; Revision 18
: CR 05-07711; NRC Procedural Concern During Performance of
: SVI-C61-T1201; dated
: November 22, 2005
: SVI-R43-T1317; Diesel Generator Start and Load Division 1; Revision 12
 
==Section 1R23: ==
: Temporary Plant Modifications Alternate Diesel Generator Starting Air Supply Temporary Modification; dated November 4, 2005
 
==Section 1EP2: ==
: Alert and Notification System (ANS) Testing The Siren Alerting System for the Perry Nuclear Power Plant; dated June 1985
: Perry Prompt Alert Siren System History; dated 1996 through 2005
: PSI-0021; Prompt Alert System; dated September 9, 2005
: Letter from FEMA [Federal Emergency Management Agency] to NRC; Perry Prompt Alert and Notification System Approval Letter; dated September 8, 1986
: PNPP [Perry Nuclear Power Plant] 6813; Prompt Alert System Annual Maintenance Checklist;
 
dated June 28 through October 14, 2004
: PNPP 6814; Prompt Alert System Maintenance Checklist; dated November 12 through
: December 17, 2004, and May 15 through June 24, 2005
: PNPP 6817; Perry Plant Prompt Alert System Repair Report; dated October 4, 2004 through
: September 24, 2005
: 2004 Emergency Planning Zone Siren System Test Schedule
: CR 05-04947; Lake County Siren Activation Failure; dated June 20, 2005
 
==Section 1EP3: ==
: Emergency Response Organization (ERO) Augmentation Testing Perry Emergency Plan; Section 6.1; Activa tion of Emergency Organizations; Revision 24
: Perry Emergency Plan; Section 8.8.4; Frequency of Drills and Exercises; Revision 24
: EPI-B1; Form PNPP 9100; Emergency Notification System Pager Messages; Revision 17
: PSI-0016; Testing of Plant Support Callout Scenarios; Revision 2
: PSI-0022; Attachments 1 and 2; Emergency Plan Training Program Course Listing and
: Requirements; Revision 0
: PTI-GEN-P0003; Quarterly Testing of the Emergency Pager System; Revision 6
: 771PYRC2005; ERO [Emergency Response Organization] Off Hours Unannounced Drill Self-Assessment Report, dated August 19, 2005
: 759PYRC2005; ERO Off Hours Unannounced Drill Self-Assessment Report; dated
: June 10, 2005
: 24PYRC2004; ERO Off Hours Unannounced Drill Self-Assessment Report; dated
: November 18, 2004
: 2RAS2004; ERO Off Hours Unannounced Drill Self-Assessment Report; dated April 2, 2004
: Perry Emergency Telephone Directory; Revision 2005-3/4
: Integrated On Call Report for Emergency Response Organization; dated December 7, 2005
: CR 05-07966; Two Radiation Protection Individuals' Qualifications Indicate Past Due and They
 
are Still in the Emergency Telephone Directory; dated December 8, 2005
: CR 05-06260; Lapsed Emergency Response Organization Qualifications; dated August 25, 2005
 
==Section 1EP4: ==
: Emergency Action Level and Emergency Plan Changes Emergency Plan for Perry Nuclear Power Plant; Revision 23
: Emergency Plan for Perry Nuclear Power Plant; Revision 22
: Emergency Plan for Perry Nuclear Power Plant; Revision 21
 
==Section 1EP5: Correction of Emergency Preparedness Weaknesses and Deficiencies==
: IPA 764PYRC2005; First Half 2005 Integrated Performance Assessment; dated August 2, 2005
: PY-C-05-03; Perry Nuclear Quality Oversight Assessment Quarterly Audit Report; dated
: November 23, 2005
: PY-C-04-04; Perry Nuclear Quality Assessment Quarterly Audit Report; dated February 17, 2005
: PY-C-04-03; Perry Nuclear Quality Assessment Quarterly Audit Report; dated November 5, 2004
: PY-C-04-02; Perry Nuclear Quality Assessment Quarterly Audit Report; dated July 23, 2004
: PY-C-04-01; Perry Nuclear Quality Assessment Quarterly Audit Report; dated April 23, 2004
: PY-C-03-04; Perry Nuclear Quality Assessment Quarterly Audit Report; dated February 4, 2004
: PY-C-03-03; Perry Nuclear Quality Assessment Quarterly Audit Report; dated October 22, 2003
: PY-C-03-02; Perry Nuclear Quality Assessment Quarterly Audit Report; dated July 22, 2003
: PY-C-03-01; Perry Nuclear Quality Assessment Quarterly Audit Report; dated March 19, 2003
: 753PYRC2005; June 20, 2005 ERO Team 'C' Training Drill Self-Assessment; dated
: July 28, 2005
: 713RAS2004; October 5, 2004, ERO Team 'A' Ev aluated Exercise Self-Assessment Report;
dated November 4, 2004
: CR 05-07313; CADAP Time Requirements in
: EPI-A1 May Not Be Met Under All Circumstances;
 
dated October 26, 2005
: CR 05-05657; Observation of Training EPlan TSC [Technical Support Center] Operation
: Manager Overall Unsat Rating; dated July 27, 2005
: CR 05-04753;
: RIS 2005-08 Endorsement NEI [Nuclear Energy Institute] Guidance for Sheltering
: Protective Action Recommendations; dated June 9, 2005
: CR 05-00107; PII B Re-Examine Respiratory Protection Qualification for ERO; dated
: January 6, 2005
: CR 04-05953; CO2 System Actuation Results in Emergency Plan Entry; dated
: November 12, 2004
 
==Section 1EP6: Drill Evaluation==
: Controller's Handbook; Team "A" ERO Drill; dated October 11, 2005
 
==Section 4OA1: ==
: Performance Indicator (PI) Verification Perry Emergency Plan; Section 7.4; Prompt Alert Siren System; Revision 24
: PYBP-RAS-0004; Appendix A; NRC Performance Indicators; Emergency Response Organization
: Drill Participation; Revision 1
: PYBP-RC-0004; Figure 1(l); NRC Performance Indicators; ERO Drill Participation, Document
 
and Data Review Form; dated July 2004 through September 2005
: PYBP-RAS-0004; Appendix A; NRC Performance Indicators; ERO Drill/Exercise Performance;
: Revision 2
: PYBP-RC-0004; Figure 1(k); NRC Performance Indicators; Emergency Preparedness
: Drill/Exercise Performance; Document and Data Review Form; dated July 2004 through
: September 2005
: PYBP-EPU-0028; Prompt Alert Siren System Emergency Planning Zone Testing; Revision 1
: PYBP-RC-0004; Figure 1(m); NRC Performance Indicators; Alert and Notification System
: Reliability; Document and Data Review Form; dated July 2004 through September 2005
: PSI-0021; Attachment 3; Prompt Alert Syst em Siren Test Reports; dated July 2004 through September 2005
: CR 05-07916; Credit Taken Incorrectly for Emergency Response Performance Indicator (DEP)
 
[Drill and Exercise Performance]; dated December 6, 2005
: CR 05-06779; Alert and Notification System Reliability Indicator Reference Data Inaccurate;
 
dated September 21, 2005
 
==Section 4OA2: Identification and Resolution of Problems==
: CR 05-07173; Declining Site Performance Noted by CAP Predictive Trending; dated October 18, 2005
: CR 05-07100; Declining Site Performance Noted by CAP Predictive Trending; dated
: October 11, 2005
: CR 05-06994; September Cognitive Trending for Maintenance Section - Work Package Errors;
 
dated October 4, 2005
: CR 05-06216; Cognitive Trend of T+6 Meeting Observations Deemed Unsatisfactory; dated
: August 19, 2005
: CR 05-06067; Containment Airlock Rework Trending; dated August 16, 2005
: CR 05-06066; Declining Trend in Procedure Use and Adherence Issues Found During Section
: IPA; dated August 16, 2005
: CR 05-06065; Declining Trend in FME Issues Found During Section Integrated Performance
: Assessment; dated August 16, 2005
: CR 05-05650; Negative Trends Identified in Emergency Planning; dated July 27, 2005
: Perry Nuclear Oversight Assessment Quarterly Audit Report
: PY-C-05-01; dated May 31, 2005
: Perry Nuclear Oversight Assessment Quarterly Audit Report
: PY-C-05-02; dated August 19, 2005
: 9
 
==Section 4OA3: Event Followup==
: LER [Licensee Event Report] 2005-003; Lack of Suction Flow Path Causes High Pressure Core Spray to be Inoperable; dated November 18, 2005
: CR 05-07435; M32 A Breaker Found Open; dated November 3, 2005
: CR 05-07442; Failure to Identify All Applicable TSs and Required Actions; dated
: November 3, 2005
==LIST OF ACRONYMS==
: [[USEDAN]] [[SAlert and Notification SystemCCCWcontrol complex chilled water]]
: [[CFR]] [[Code of Federal Regulations]]
CRcondition reportDCdirect current
ECCemergency closed cooling
EDGemergency diesel generator
EPEmergency Preparedness
EPIemergency implementing procedures
EROEmergency Response Organization
ESWemergency service water
FPIFire Protection Instruction
FSARFinal Safety Analysis Report
FENOCFirstEnergy Nuclear Operating Company
HPCShigh pressure core spray
IMCInspection Manual Chapter
LERLicensee Event Report
NCVnon-cited violation
NRCNuclear Regulatory Commission
ONIOff-Normal Instruction
OWAoperator work around
PAPPerry Administrative Procedure
PIPerformance Indicator
PMIPreventive Maintenance Instruction
PMTpost-maintenance testing
RHRresidual heat removal
SDPsignificance determination process
SSCstructures, systems, and components
SVIsurveillance instruction
TBCCWTurbine Building Closed Cooling Water
TSTechnical Specification
USARUpdated Safety Analysis Report
VLIvalve lineup instruction
: [[WO]] [[work order]]
}}

Revision as of 03:29, 29 October 2018

IR 05000440-05-010; 10/1/2005-12/31/2005; Perry Nuclear Power Plant; Post-Maintenance Testing
ML060380729
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 02/07/2006
From: Satorius M A
Division Reactor Projects III
To: Pearce W H
FirstEnergy Nuclear Operating Co
References
IR-05-010
Download: ML060380729 (40)


Text

February 7, 2006

Mr. Acting Vice President

FirstEnergy Nuclear Operating Company

Perry Nuclear Power Plant

10 Center Road, A290

Perry, OH 44081

SUBJECT: PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 05000440/2005010

Dear Mr. Pearce:

On December 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection

findings that were discussed on January 6, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel. In addition to the routine NRC inspection and assessment activities, Perry

performance is being evaluated quarterly as described in the Assessment Follow-up Letter -

Perry Nuclear Power Plant, dated August 12, 2004. Consistent with Inspection Manual Chapter (IMC) 0305, "Operating Reactor Assessment Progr am," plants in the "Multiple/Repetitive Degraded Cornerstone" column of the NRC's Action Matrix are given consideration at each

quarterly performance assessment review for (1) declaring plant performance to be unacceptable

in accordance with the guidance in IMC 0305; (2) transferring to the IMC 0350, "Oversight of

Operating Reactor Facilities in a Shutdown Condi tion with Performance Problems," process; and (3) taking additional regulatory actions, as appropriate. On December 1, 2005, the NRC

reviewed Perry operational performance, inspection findings, and performance indicators for the

third quarter of 2005. Based on this review, we concluded that Perry is operating safely. We

determined that no additional regulatory actions, beyond the already increased inspection

activities and management oversight, are currently warranted.

Based on the results of this inspection, three findings of very low safety significance, all of which involved violations of NRC requirements, we re identified. However, because of their very low safety significance and because they have been entered into your corrective action program, the NRC is treating these violations as non-cited violations (NCVs) in accordance with

Section VI.A.1 of the NRC's Enforcement Policy.

W. Pearce-2-

If you contest the subject or severity of these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Perry Nuclear Power Plant.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Ava ilable Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/Mark A. Satorius, Director Division of Reactor Projects Docket No. 50-440 License No. NPF-58

Enclosure:

Inspection Report 05000440/2005010

w/Attachment:

Supplemental Informationcc w/encl:G. Leidich, President - FENOC J. Hagan, Chief Operating Officer, FENOC

D. Pace, Senior Vice President Engineering and Services, FENOC

Director, Site Operations

Director, Regulatory Affairs

M. Wayland, Director, Maintenance Department

Manager, Regulatory Compliance

T. Lentz, Director, Performance Improvement

J. Shaw, Director, Nuclear Engineering Department

D. Jenkins, Attorney, First Energy

Public Utilities Commission of Ohio

Ohio State Liaison Officer

R. Owen, Ohio Department of Health

SUMMARY OF FINDINGS

IR 05000440/2005010; 10/1/2005-12/31/2005; Perry Nuclear Power Plant; Post-Maintenance

Testing This report covers a 3-month period of baseline inspection. The inspection was conducted by the resident and regional inspectors. This inspection identified three Green findings, all of which involved associated non-cited violations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, "Significance

Determination Process". Findings for which the Significance Determination Process does not apply may be "Green" or be assigned a severity level after NRC management review. The

NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.

NRC-Identified

and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance and an associated non-cited violation of Technical Specification 5.4, "Procedures," was self-revealed during Division 2 Emergency

Diesel Generator (EDG) post-maintenance testing on September 15, 2005, when the engine-driven fuel oil pump was discovered air bound after licensee personnel failed to implement appropriate procedures for the fill and vent of the pump suction and discharge lines following pump maintenance activities. As a result of operating the pump for about 40 minutes without proper fuel oil flow, the engine-driven fuel oil pump required replacement, which extended the Division 2 EDG maintenance outage by about 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and incurred about 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> of unnecessary unavailability. As part of their corrective actions, the licensee removed the EDG from service, replaced the engine-driven fuel oil pump, and successfully re-tested the EDG on September 16, 2005. The primary cause of this finding was related to the cross-cutting area of Human Performance since licensee personnel failed to develop an appropriate fill and vent procedure for the engine-driven fuel oil pump.

This finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low safety significance because: (1) it did not represent an actual loss of safety function of a system; (2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time; (3) it did not represent an actual loss of safety function of one or more non-Technical Specification trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and (4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event. (Section 1R19.1)*Green. A finding of very low safety significance and an associated non-cited violation of Technical Specification 5.4, "Procedures," was self-revealed on October 30, 2005, when licensee personnel failed to develop an appropriate procedure for the replacement of the

'B' Emergency Closed Cooling (ECC) pump oil bearing reservoir, which resulted in an oil leak and unnecessary pump unavailability. As part of their corrective actions, licensee personnel completed repairs to the pump on November 1, 2005, which included establishing a correct reservoir height and performing post-maintenance testing with satisfactory results. The primary cause of this finding was related to the cross-cutting area of Human Performance because licensee personnel failed to develop appropriate oil reservoir maintenance procedures.

This finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low safety significance because: (1) it did not represent an actual loss of safety function of a system; (2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time; (3) it did not represent an actual loss of safety function of one or more non-Technical Specification trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and (4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event. (Section 1R19.2)*Green. A finding of very low safety significance and an associated non-cited violation of10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," was self-revealed on

November 19, 2005, when licensee personnel failed to promptly correct a condition adverse to quality associated with the development of appropriate procedures for oil reservoir replacement, which resulted in an oil leak on the 'A' ECC pump, incurring unnecessary pump unavailability. As part of their corrective actions, licensee personnel completed repairs to the pump on November 29, 2005, which included establishing a correct reservoir height and performing post-maintenance testing with satisfactory results.

The primary cause of this finding was related to the cross-cutting area of Problem

Identification and Resolution because licensee personnel failed to correct an inadequate oil reservoir maintenance procedure in a timely manner.

This finding was more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low safety significance because: (1) it did not represent an actual loss of safety function of a system; (2) it did not represent an actual loss of safety function of a single train for greater than its Technical Specification allowed outage time; (3) it did not represent an actual loss of safety function of one or more non-Technical Specification trains of equipment designated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and (4) it did not screen as potentially risk significant due to a seismic, fire, flooding, or severe weather initiating event. (Section 1R19.3)

4

B. Licensee-Identified Violations

Three violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.

5

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period at 100 percent power. On October 8, 2005, operators reduced reactor power to 95 percent to isolate a main condenser train to address a condenser

tube leak and returned to 100 percent power later the same day. On October 12, 2005, operators reduced reactor power to 65 percent in order to perform a condenser tube repair and

control rod sequence exchange. After several power maneuvers for rod alignment, operators returned the reactor to 100 percent power on October 15, 2005. The plant remained at

100 percent power for the remainder of the inspection period with the exception of planned

downpowers for routine surveillance testing and rod sequence exchanges.1.REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and Emergency Preparedness1R01Adverse Weather Protection (71111.01)

a. Inspection Scope

The inspectors reviewed the licensee's procedures and preparations for cold weather conditions. The inspectors reviewed winterization procedures, severe weather

procedures, and performed general area walkdowns. During walkdowns conducted the

week of October 17, 2005, the inspectors toured selected buildings and areas to

determine whether the licensee had identified all discrepant conditions such as damaged

doors, windows, or vent louvers. The inspectors reviewed documentation to determine

whether licensee procedure PTI-GEN-P0026, "Preparations For Winter Operation,"

Revision 2, had been completed prior to the onset of cold weather. Additionally, the

inspectors observed housekeeping conditions and verified that materials capable of

becoming airborne missile hazards during high wind conditions, or impacting snow

removal, were appropriately located and restrained. Finally, the inspectors reviewed the

licensee's cold weather readiness to determine whether cold weather protection features

such as heat tracing and space heaters were monitored and functional.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

a. Inspection Scope

The inspectors conducted partial walkdowns of the system trains listed below to determine whether the systems were correctly aligned to perform their designed safety 6 function. The inspectors used licensee valve lineup instructions (VLIs) and system drawings during the walkdowns. The walkdowns included selected switch and valve

position checks, and verification of electrical power to critical components. Finally, the

inspectors evaluated other elements, such as material condition, housekeeping, and

component labeling. The documents used for the walkdowns are listed in the attached

List of Documents Reviewed. The inspectors reviewed the following systems:*the Control Complex Chilled Water (CCCW) system 'B' while CCCW 'A' was unavailable due to planned maintenance during the week of October 3, 2005; and*the Division 1 Emergency Diesel Generator (EDG) and support systems on November 16, 2005, following completion of a Division 1 maintenance outage.

These reviews represented two inspection samples.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05AQ)

a. Inspection Scope

The inspectors walked down the following areas to assess the overall readiness of fire protection equipment and barriers:*Fire Zone 1DG-1A, Unit 1 Division 2 Diesel Generator Building elevation 620'-6" and 646'-6";*Fire Zone 1DG-1C, Unit 1 Division 1 Diesel Generator Building elevation 620'-6" and 646'-6";*Fire Zone 1AB-1A, Unit 1 - Low Pressure Core Spray System;

  • the turbine building (all zones); and
  • the heater bay (all zones).

Emphasis was placed on evaluating the licensee's control of transient combustibles and ignition sources, the material condition of fire protection equipment, and the material

condition and operational status of fire barriers used to prevent fire damage or

propagation. The inspectors utilized the general guidelines established in licensee

procedures Fire Protection Instruction (FPI)-A-A02, "Periodic Fire Inspections,"

Revision 3; Perry Administrative Procedure (PAP)-1910, "Fire Protection Program,"

Revision 11; and PAP-0204, "Housekeeping/Cleanliness Control Program," Revision 15;

as well as basic National Fire Protection Association Codes, to perform the inspection

and to determine whether the observed conditions were consistent with procedures and

codes.The inspectors observed fire hoses, sprinklers, and portable fire extinguishers to determine whether they were installed at their designated locations, were in satisfactory

physical condition, and were unobstructed. The inspectors also evaluated the physical

location and condition of fire detection devices. Additionally, passive features such as fire 7 doors, fire dampers, and mechanical and electrical penetration seals were inspected to determine whether they were in good physical condition. The documents listed at the

end of this report were used by the inspectors during the assessment of this area.

These reviews represented five inspection samples.

b. Findings

No findings of significance were identified.

1R07 Heat Sink (71111.07)

a. Inspection Scope

The inspectors reviewed Residual Heat Removal (RHR) 'A' and RHR 'C' heat exchanger performance testing conducted December 1, 2005. The inspectors reviewed the

licensee's preliminary test results and reviewed historical trending data to verify that

current testing frequency was sufficient to detect degradation of heat exchanger

performance.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11).1Annual Operating Test Results

a. Inspection Scope

The inspector reviewed the overall pass/fail results of the annual operating examination, which consisted of Job Performance Measure (JPM) and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee. The

operating testing was conducted in November and December 2005. The results were

compared with the significance determination process in accordance with NRC Manual

Chapter 0609, Appendix I, "Operator Requalification Human Performance Significance

Determination Process (SDP)."

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

8.2 Quarterly Inspection

a. Inspection Scope

On November 22, 2005, the resident inspectors observed licensed operator performance in the plant simulator. The inspectors evaluated crew performance in the areas of:*clarity and formality of communication;*ability to take timely action in the safe direction;

  • prioritizing, interpreting, and verifying alarms;
  • correct use and implementation of procedures, including alarm response procedures;*timely control board operation and manipulation, including high-risk operator actions; and,*group dynamics.

The inspectors also reviewed the licensee's evaluation of crew performance to determine whether the training staff had identified performance deficiencies and specified

appropriate remedial actions.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the licensee's implementation of the maintenance rule requirements to determine whether component and equipment failures were identified

and scoped within the maintenance rule and that select structures, systems, and

components (SSCs) were properly categorized and classified as (a)(1) or (a)(2) in

accordance with 10 CFR 50.65. The inspectors reviewed station logs, maintenance work

orders (WOs), selected surveillance test procedures, and a sample of condition reports (CRs) to determine whether the licensee was identifying issues related to the

maintenance rule at an appropriate threshold and that corrective actions were

appropriate. Additionally, the inspectors reviewed the licensee's performance criteria to

determine whether the criteria adequately monitored equipment performance and to

determine whether licensee changes to performance criteria were reflected in the

licensee's probabilistic risk assessment. During this inspection period, the inspectors

reviewed the following SSCs:*the DC (direct current) electrical system; *the electrical switchyard; and

9 These reviews represented three inspection samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation of plant risk, scheduling, configuration control, and performance of maintenance associated with planned and emergent work

activities to determine whether scheduled and emergent work activities were adequately

managed in accordance with 10 CFR 50.65(a)(4). In particular, the inspectors reviewed

the licensee's program for conducting maintenance risk assessments to determine

whether the licensee's planning, risk management tools, and the assessment and

management of on-line risk were adequate. The inspectors also reviewed licensee

actions to address increased on-line risk when equipment was out of service for

maintenance, such as establishing compensatory actions, minimizing the duration of the

activity, obtaining appropriate management approval, and informing appropriate plant staff, to determine whether the actions were accomplished when on-line risk was

increased due to maintenance on risk-significant SSCs. The following assessments

and/or activities were reviewed:*the licensee's management of emergent work activities associated with a high pressure condenser tube leak and planned switchyard activities during the week

of October 10, 2005;*the maintenance risk assessment and risk management actions associated with emergent work on the Division 2 EDG governor control switch on

October 18, 2005;*the licensee's risk management of work activities associated with the Division 1 EDG extended outage during the weeks of October 31, 2005, and

November 7, 2005;*the maintenance risk assessment and risk management actions associated with the replacement of the Division 2 EDG jacket water cooling pump on

December 7, 2005; and*the licensee's risk management of work activities associated with planned maintenance of the Emergency Closed Cooling (ECC) 'B' Pump on December 27, 2005.These reviews represented five inspection samples.

b. Findings

No findings of significance were identified.

101R14Operator Performance During Non-Routine Evolutions and Events (71111.14).1Condenser Tube Leak

a. Inspection Scope

The inspectors reviewed the licensee's response to increasing condensate conductivity on October 7, 2005. The inspectors reviewed the licensee's immediate and supplemental

actions to determine whether they were consistent with actions specified in licensee Off-

Normal Instruction (ONI)-N61, "Condenser Tube Leak/Organic Intrusion," Revision 9. The

inspectors also observed licensee actions associated with leak isolation and repair.

This review represented the first of two inspection samples.

b. Findings

No findings of significance were identified..2Offgas Building Radiation Monitor Alarms

a. Inspection Scope

The inspectors observed the licensee's response to offgas building radiation monitor alarms during maintenance on the offgas system on December 21, 2005. The inspectors

observed the licensee's immediate and supplemental actions to determine whether they

were consistent with actions specified in ONI-D17, "High Radiation Levels Within Plant,"

Revision 10.

This review represented the second of two inspection samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors selected CRs related to potential operability issues for risk-significant components and systems. These CRs were evaluated to determine whether the

operability of the components and systems was justified. The inspectors compared the

operability and design criteria in the appropriate sections of the Technical Specifications (TS) and Updated Safety Analysis Report (USAR) to the licensee's evaluations, to

determine whether the components or system s were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the

measures were in place, would function as intended, and were properly controlled.

Additionally, the inspectors determined, where appropriate, compliance with bounding 11 limitations associated with the evaluations. The inspectors reviewed the following issues:*the licensee's conclusions regarding the operability of the Division 1 EDG after the identification of a 25 drop-per-minute jacket water leak on October 5, 2005;*the licensee's assessment of the affect of degrading Division 2 EDG jacket water keep-warm pump seal leakage on Division 2 EDG operability on

October 25, 2005;*the licensee's justification for an operability determination request after identifying an oil leak associated with the ECC 'B' pump on October 30, 2005; and*the licensee's evaluation of nonconforming conditions associated with the EDG exhaust corridor heat shield during the week of November 7, 2005.

These reviews represented four inspection samples.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds (71111.16)

a. Inspection Scope

During the week ending October 15, 2005, the inspectors performed a semiannual review of the cumulative effects of operator workarounds (OWAs). The list of open OWAs was

reviewed to identify any potential effect on the functionality of mitigating systems.

Inspection activities included, but were not limited to, a review of the cumulative effects of

the OWA on the availability and the potential for improper operation of the system, for

potential impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents. Additionally, the inspectors conducted a review of recent CRs to

ensure that OWA related issues were entered into the corrective action program when

required.This review represented one inspection sample.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors evaluated the following post-maintenance testing (PMT) activities for risk-significant systems to assess the following (as applicable): the effect of testing on

the plant had been adequately addressed; testing was adequate for the maintenance

performed; acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate; tests were performed as written; and equipment was

returned to its operational status following testing. The inspectors evaluated the activities 12 against TS, the USAR, 10 CFR 50 requirements, licensee procedures, and various NRC generic communications. In addition, the inspectors reviewed CRs associated with PMTs

to determine whether the licensee was identifying problems and entering them in the

corrective action program. The specific procedures and CRs reviewed are listed in the

attached List of Documents Reviewed. The following post-maintenance activities were

reviewed:*testing of the Division 1 EDG following planned maintenance on September 14, 2005;*testing of the CCCW 'A' system following maintenance on October 6, 2005;

  • testing of the Division 2 EDG governor control switch following switch replacement on October 18, 2005;*testing of the Division 1 EDG logic control board following replacement on November 9, 2005; and*testing of the ECC 'A' pump following emergent maintenance conducted November 29, 2005.

These reviews represented five inspection samples.

b. Findings

.1Inadequate Fill and Vent Procedure Resulted in Division 1 EDG Unavailability Introduction

A finding of very low safety significance (Green) and an associated non-cited violation (NCV) of TS 5.4, "Procedures," was self-revealed during Division 2

EDG post-maintenance testing on September 15, 2005, when the engine-driven fuel oil

pump was discovered air bound after licensee personnel failed to develop appropriate

procedures for the fill and vent of the engine-driven fuel oil pump suction and discharge

lines following pump maintenance activities. As a result of operating the pump for about

40 minutes without proper fuel oil flow, the engine-driven fuel oil pump required

replacement, which extended the Division 2 EDG maintenance outage by about 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

and incurred about 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> of unnecessary unavailability.

Description

On September 14, 2005, the licensee commenced a planned Division 2 maintenance outage. Planned maintenance activities included the Division 2 EDG and

EDG support systems, including the fuel oil system. Licensee personnel completed EDG

maintenance on September 15, 2005, and after restoring EDG support systems, the

licensee declared the EDG available. The licensee commenced post-maintenance EDG

testing at about 5:45 p.m. During the test, the "FUEL PUMP/OS DRIVE FAILURE" alarm

was received shortly after the EDG was started and the EDG was stopped in accordance

with the governing alarm response instruction. Subsequently, on September 16, 2005, the EDG was again started at 00:54 a.m. to obtain additional data. The "FUEL PUMP/OS

DRIVE FAILURE" alarm was again received and pump discharge pressure was noted to

be only about 5 pounds per square inch gauge (psig). The licensee removed the EDG

from service, replaced the engine-driven fuel oil pump, and successfully tested the EDG.

The EDG was declared available at 6:43 p.m. on September 16, 2005 after successful

post-maintenance testing and declared operable later that same day.

13 Subsequent licensee review identified that the fill and vent procedure specified in Section 0600, step 2, of WO 200135325, dated September 14, 2005, which was used to

restore the fuel oil system, was inadequate since the use of the direct current (DC) fuel oil

booster pump to prime the system did not fill piping upstream of the engine-driven fuel oil pump discharge check valves. The inspectors determined that failure to develop

appropriate procedures for the fill and vent of the engine-driven fuel oil pump suction and

discharge lines was a performance deficiency warranting a significance determination.

Analysis:

The inspectors concluded that the finding was greater than minor in accordance with Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports," dated September 30, 2005. The finding was associated with the Mitigating

Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, licensee personnel

failed to develop an appropriate procedure for the fill and vent of the engine-driven fuel oil

pump suction and discharge lines that extended the Division 2 EDG maintenance outage

by about 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and incurred about 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> of unnecessary Division 2 EDG

unavailability. The finding also affected the cross-cutting area of Human Performance

since licensee personnel failed to develop an appropriate fill and vent procedure.

The inspectors completed a significance determination of this issue using Appendix A,"Determining the Significance of Reactor Inspection Findings for At-Power Situations," of

IMC 0609, "Significance Determination Process (SDP)," dated November 22, 2005. The

inspectors determined that the issue was of very low safety significance, in accordance

with the Phase 1 screening worksheet, because:

(1) it did not represent an actual loss of

safety function of a system;

(2) it did not represent an actual loss of safety function of a

single train for greater than its TS allowed outage time;

(3) it did not represent an actual

loss of safety function of one or more non-TS trains of equipment designated as

risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and

(4) it did not screen as

potentially risk significant due to a seismic, fire, flooding, or severe weather initiating

event.Enforcement

Technical Specification 5.4, "Procedures," requires, in part, that written procedures be implemented covering applicable procedures recommended by Regulatory

Guide 1.33, "Quality Assurance Program Requirements (Operation)," Revision 2, dated

February 1978. Regulatory Guide 1.33, Appendix A, paragraph 9a, stated, "Maintenance

that can affect the performance of safety-related equipment should be properly

preplanned and performed in accordance with written procedures, documented

instructions, or drawings appropriate to the ci rcumstances." Contrary to this requirement, the licensee failed to implement procedures that were appropriate to the circumstances in

that the instructions provided in Section 0600, step 2, of WO 200135325, dated

September 14, 2005, resulted in an inadequate fill and vent of the Division 2 EDG engine-

driven fuel oil pump suction and discharge lines following maintenance. However, because of the very low safety significance of the issue and because the issue has been

entered into the licensee's corrective action program (CR 05-06668), the issue is being

treated as a non-cited violation (NCV) consistent with Section VI.A.1 of the NRC

Enforcement Policy (NCV 05000440/2005010-01).

14 As part of their corrective actions, licensee personnel removed the EDG from service, replaced the engine-driven fuel oil pump, and successfully re-tested the EDG on

September 16, 2005..2Inappropriate Procedure Implementation Resulted in 'B' ECC Pump Unavailability Introduction

A finding of very low safety significance (Green) and an associated NCV of TS 5.4, "Procedures," was self-revealed on October 30, 2005, when licensee personnel

failed to develop an appropriate procedure for the replacement of a 'B' Emergency

Closed Cooling (ECC) pump oil reservoir, which resulted in an oil leak and incurred

unnecessary pump unavailability.

Description

On September 14, 2005, licensee personnel performed maintenance on the

'B' ECC pump that installed a re-designed Trico oil reservoir on the inboard and outboard

pump bearings. Subsequently, licensee operating logs documented oil additions to the

'B' ECC pump on September 28, 2005, and October 30, 2005.

On October 29, 2005, licensee personnel determined that the pump leaked oil when in operation. Licensee personnel questioned the ability of the pump to perform its design

basis function, subsequently declared the pump inoperable, and removed the pump from

service for repair. Licensee personnel replaced the pump outboard bearing seal to

address the oil leakage. On October 31, 2005, the licensee conducted post-maintenance

testing and noted that the pump continued to leak oil. After further investigation, licensee

personnel determined that the reservoir replacement maintenance activity had resulted in

an incorrect installation height for the pump outboard bearing oil reservoir. This resulted

in a higher than required oil level in the pump and led to increased pump temperature and

seal leakage. As part of their corrective actions, licensee personnel completed repairs to

the pump on November 1, 2005, which included establishing a correct reservoir height

and performing post-maintenance testing with satisfactory results.

The inspectors reviewed WO 200075252 that was used to replace the 'B' ECC pump bearing oil reservoirs on September 14, 2005.

The WO prescribed the use of Preventive Maintenance Instruction (PMI)-0050, "Preventive Maintenance Lubricating Guidelines,"

Revision 3, to install the reservoir. Section 5.3.2 of PMI-0050, "Opto-Matic Oiler Bottles (Motors, Pumps, Gear Reducers, ect. [sic])," referenced Attachment 2, "Plastic

Opto-Matic Oilers," for guidance. Attachm ent 2 was a copy of the September 1989 Trico manufacturer's instructions for installation of Opto-Matic oilers. Attachment 2, step 8, instructed operators to start the machine after oil reservoir installation and observe

whether proper oil level was maintained. If oil was not at the proper level, the instruction

returned operators to steps 6 and 7 for additional oil reservoir height adjustments.

However, the inspectors noted that Section 5.3.2 of PMI-0050 stated that Attachment 2 "may be referred to for guidance on Opto-matic oiler (oil reservoir) alignment," and, as

such, the instructions were optional. Section 5.3.2 only required operators to install the

reservoir, add oil, and then run the pump for 10 minutes and note any oil leakage.

Section 5.3.2 contained no steps to check for proper oil level after oil was added to the

pump or after the pump was run. The inspectors noted that the procedure steps in

Section 5.3.2 were inconsistent with the vendor guidance in Attachment 2 to check for 15 proper oil level after oil reservoir installation and pump run to verify that the reservoir height was correct. The licensee's performance of PMI-0050 resulted in an incorrect

reservoir installation height at the completion of the maintenance. The licensee's post-

maintenance testing failed to detect the flawed condition.

The licensee concluded that improper installation of the oil reservoir for the 'B' ECC outboard pump bearing led to an oil level that was about 1/4-inch too high. This resulted

in an oil leak from the bearing seal.

The inspectors determined that the licensee's failure to implement appropriate procedures for the replacement of the oil reservoir on September 14, 2005, which

resulted in pump oil leakage and unavailability when the pump was removed from service for necessary repairs, was a performance deficiency warranting a significance evaluation.

Analysis:

The inspectors concluded that the finding was greater than minor in accordance with Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports," dated September 30, 2005. Specifically, the finding was associated with the

Mitigating Systems cornerstone attribute of equipment performance and affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. The improper pump oil

reservoir installation resulted in an oil leak and unnecessary pump unavailability. The

finding affected the cross-cutting area of Human Performance because licensee

personnel failed to develop appropriate procedures for the oil reservoir replacement

activity.The inspectors completed a significance determination of this issue using Appendix A,"Determining the Significance of Reactor Inspection Findings for At-Power Situations," of

IMC 0609, "Significance Determination Process (SDP)," dated November 22, 2005. The

inspectors determined that the finding was of very low safety significance, in accordance

with the Phase 1 screening worksheet, because:

(1) it did not represent an actual loss of

safety function of a system;

(2) it did not represent an actual loss of safety function of a

single train for greater than its TS allowed outage time;

(3) it did not represent an actual

loss of safety function of one or more non-TS trains of equipment designated as

risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and

(4) it did not screen as

potentially risk significant due to a seismic, fire, flooding, or severe weather initiating

event.Enforcement

Technical Specification 5.4, "Procedures," required the implementation of the applicable procedures recommended in Regulatory Guide 1.33, "Quality Assurance

Program Requirements (Operation)," Revision 2, dated February 1978. Regulatory Guide

1.33 Appendix A, Part 9a, stated, "Maintenance that can affect the performance of safety-

related equipment should be properly preplanned and performed in accordance with

written procedures, documented instructions, or drawings appropriate to the

circumstances." Contrary to this r equirement, the licensee failed to implement procedures that were appropriate to the circumstances during the replacement of the

'B' ECC pump outboard bearing oil reservoir on September 14, 2005, which resulted in

an incorrect reservoir installation height and an oil leak that led to unnecessary pump

inoperability and unavailability. However, because of the very low safety significance of 16 the issue and because the issue has been entered into the licensee's corrective action program (CR 05-07379), the issue is being treated as a non-cited violation (NCV)

consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000440/20050010-02).

As part of the licensee's corrective actions, on November 1, 2005, the licensee established a correct oil reservoir height and performed post-maintenance testing with satisfactory results..3Failure to Correct an Identified Procedure Issue Resulted in 'A' ECC Pump Unavailability Introduction

A finding of very low safety significance (Green) and an associated NCV of10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," was self-revealed on

November 19, 2005, when licensee personnel failed to promptly correct a condition

adverse to quality associated with the development of appropriate procedures for oil

reservoir replacement, which resulted in an oil leak on the 'A' ECC pump and

unnecessary pump unavailability.

Description

On September 14, 2005, licensee personnel performed maintenance on the

'B' ECC pump that installed a re-designed Trico oil reservoir on the inboard and outboard

pump bearings. The pump subsequently leaked oil and was declared inoperable and

unavailable. The licensee performed maintenance to replace the pump shaft seal to

address the oil leakage. Following this maintenance, the licensee noted that the pump

continued to leak oil. On October 31, 2005, the licensee identified that the reservoir

replacement maintenance activity had resulted in an incorrect reservoir installation height

and that this caused the pump to leak oil. Revision 3 of PMI-0050, "Preventive

Maintenance Lubricating Guidelines," was the procedure used to install the reservoir.

On November 3, 2005, the licensee performed maintenance on the 'A' ECC pump that installed the revised Trico oil reservoir design. Licensee personnel used the same

procedure, PMI-0050, Revision 3, to install the reservoir. The pump leaked oil during

post-maintenance testing on November 5, 2005, and the licensee determined that this

was the result of an incorrect oil reservoir installation height. The licensee performed an

adjustment to the reservoir height and declared the pump operable.

Subsequently, the November 19, 2005, operator log entries identified that oil was "being slung from the shaft" of the 'A' ECC pump. On November 20, 2005, operators declared

the 'A' ECC pump inoperable and shut it down for maintenance. On pump shutdown, the

operator logs identified that the inboard bearing was "spraying a mist of oil" and that the

reservoir oil level was "at the bottom of the glass." The licensee identified that the

leakage was due to an incorrect oil reservoir height adjustment on the inboard bearing, performed work to correct the condition, and declared the pump operable later the same

day.Subsequently on November 28, 2005, the licensee declared the 'A' ECC pump inoperable due to oil leakage from the outboard bearing. The licensee determined that

this was caused by an improper oil reservoir height on the outboard bearing. As part of

their corrective actions, licensee personnel completed repairs to the pump on 17 November 29, 2005, which included establishing a correct reservoir height and performing post-maintenance testing with satisfactory results.

The inspectors noted that the licensee had also performed work to replace the oil reservoirs on the 'A' Turbine Building Closed Cooling Water (TBCCW) pump, a

safety-significant pump. This again produced improper oil reservoir installations. On

November 15, 2005, the pump reservoirs were replaced. On November 16, 2005, significant oil leakage was noted from the 'A' TBCCW pump and the operator logs

identified that the outboard bearing oil reservoir was empty. Condition Report 05-07633, "TBCC Pump A Failed PMT," dated November 16, 2005, stated that "oil covered the floor

in the Turbine Building." Work was performed to address an improper oil reservoir

installation on the pump the same day. Subsequently, on November 19, 2005, the 'A'

TBCCW pump was again noted to be leaking oil due to an incorrect reservoir height. The

licensee repaired the pump on November 22, 2005, with satisfactory results.

In summary, the licensee identified that the performance of the oil reservoir replacement maintenance procedure in PMI-0050, Revision 3, resulted in incorrect oil reservoir

installations on the 'B' ECC pump. The licensee then subsequently performed the same

procedure on other equipment and caused degraded conditions on the 'A' ECC and

'A' TBCCW pumps. Additionally, initial post-maintenance testing for both the 'A' ECC

and the 'A' TBCCW pumps identified that the maintenance had resulted in improper

reservoir installation height. This provided an additional opportunity to address the

appropriateness of the reservoir maintenance procedure prior to returning the equipment

to service. Therefore, the inspectors determined that reasonable opportunities existed to

address the reservoir maintenance issues before performing work on additional

safety-related or safety-significant system s, and before returning equipment to service with a degraded condition. The inspectors determined that the failure to promptly correct

the deficiencies associated with the reservoir maintenance procedures was a

performance deficiency warranting a significance evaluation.

Analysis:

The inspectors concluded that the finding was greater than minor in accordance with Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports," dated September 30, 2005. Specifically, the finding was associated with the

Mitigating Systems cornerstone attribute of equipment performance and affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. The failure to promptly

correct deficiencies in the reservoir maintenance procedure led to additional safety

system degradation and unavailability. The finding affected the cross-cutting area of

Problem Identification and Resolution because licensee personnel failed to promptly

correct the deficiencies associated with the reservoir maintenance procedure in a timely

manner, which resulted in additional incorrect reservoir installations.

The inspectors completed a significance determination of this issue using Appendix A,"Determining the Significance of Reactor Inspection Findings for At-Power Situations," of

IMC 0609, "Significance Determination Process (SDP)," dated November 22, 2005. The

inspectors determined that the issue was of very low safety significance, in accordance

with the Phase 1 screening worksheet, because:

(1) it did not represent an actual loss of

safety function of a system;

(2) it did not represent an actual loss of safety function of a 18 single train for greater than its TS allowed outage time;
(3) it did not represent an actual loss of safety function of one or more non-TS trains of equipment designated as

risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and

(4) it did not screen as

potentially risk significant due to a seismic, fire, flooding, or severe weather initiating

event.Enforcement: 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly

identified and corrected. Contrary to this requirement, on October 31, 2005, during

maintenance on the 'B' ECC pump, licensee personnel identified that oil reservoir

maintenance procedure PMI-0050, "Preventive Maintenance Lubricating Guidelines,"

Revision 3, was inadequate in that it resulted in an incorrect reservoir installation height.

The licensee failed to correct the procedure in a timely manner and, as a result, on

November 3, 2005, applied the same procedure to the 'A' ECC pump, resulting in

unnecessary pump inoperability and unavailability. However, because of the very low

safety significance of the issue and because the issue has been entered into the

licensee's corrective action program (CR 05-07688), the issue is being treated as an NCV

consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000440/20050010-03).

As part of their corrective actions, licensee personnel completed repairs to the pump on November 29, 2005, which included establishing a correct reservoir height and

performing post-maintenance testing with satisfactory results.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed surveillance testing or reviewed test data for risk-significant systems or components to assess compliance with TS; 10 CFR 50, Appendix B; and

licensee procedure requirements. The testing was also evaluated for consistency with

the USAR. The inspectors verified that the testing demonstrated that the systems were

ready to perform their intended safety functions. The inspectors determined whether test

control was properly coordinated with the control room and performed in the sequence

specified in the surveillance instruction (SVI), and if test equipment was properly

calibrated and installed to support the surveillance tests. The procedures reviewed are

listed in the attached List of Documents Reviewed. The surveillance activities assessed

were:*main steam isolation valve and logic functional testing conducted October 22, 2005;*CCCW 'B' pump and valve testing conducted October 28, 2005;

  • remote shutdown panel control operability test for RHR 'A,' ESW 'A,' and ECC 'A' conducted during the week of October 31, 2005;*high pressure core spray (HPCS) pump and valve operability test on November 15, 2005;*the Division 1 EDG monthly surveillance conducted December 28, 2005.

19 These reviews represented five inspection samples.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the documentation for a contingency temporary configuration change associated with installation of an alternate air charging system for the Division 2

EDG. The inspectors reviewed the temporary configuration change and the

10 CFR 50.59 screening and evaluation information against the design basis, the USAR

and the TS as applicable. The inspectors walked down the locations of all staged

equipment associated with this modification to determine whether plant safety systems were adversely impacted.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.1EP2Alert and Notification System Testing (71114.02)

a. Inspection Scope

The inspectors discussed with Emergency Preparedness (EP) staff the operation, maintenance, and periodic testing of the Alert and Notification System (ANS) in the Perry

Nuclear Power Plant's plume pathway Emergency Planning Zone to determine whether

the ANS equipment was adequately maintained and tested in accordance with

Emergency Plan commitments and procedures. The inspectors reviewed records of

2004 and 2005 preventative, non-scheduled maintenance activities and weekly

operability test results.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.1EP3Emergency Response Organization Augmentation Testing (71114.03)

a. Inspection Scope

20 The inspectors reviewed and discussed with plant EP staff the emergency plan commitments, emergency implementing procedures (EPI), and other instructions that

addressed the primary and alternate methods of initiating an Emergency Response

Organization (ERO) activation to augment the on-shift ERO, as well as the provisions for

maintaining the plant's ERO call-out roster and emergency telephone directory. The

inspectors also reviewed reports and a sample of corrective action program records of

unannounced off-hour augmentation tests, which were conducted in 2004 and 2005, to

determine the adequacy of the drills' critiques and associated corrective actions. The

inspectors also reviewed the EP training records of a sample of 17 Perry Power Plant

ERO personnel, who were assigned to key and support positions, to determine whether

they were currently trained for their assigned ERO positions.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.1EP4Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspectors performed a screening review of portions of Revisions 22 and 23 of the Perry Nuclear Plant Emergency Plan to determine whether the changes made in these

revisions decreased the effectiveness of the licensee's emergency planning. This

screening review did not constitute an approval of the changes and, as such, the changes

are subject to future NRC inspection to ensure that the emergency plan continues to

meet NRC regulations.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a. Inspection Scope

The inspectors reviewed Nuclear Oversight staff's 2004 and 2005 reviews of the licensee's EP program to verify that these independent assessments met the

requirements of 10 CFR 50.54(t). The inspectors reviewed a sample of CR records

associated with those reviews to determine whether Nuclear Oversight concerns were

being addressed. The inspectors also reviewed critique reports and samples of CR

records associated with the 2004 biennial exercise in order to verify that the licensee

fulfilled its annual drill commitments and to evaluate the licensee's efforts to adequately

identify, track, and resolve concerns identified during these activities.

21 These activities represented one inspection sample.

b. Findings

No findings of significance were identified.1EP6Drill Evaluation (71114.06)

a. Inspection Scope

The inspectors observed activities in the simulator control room, the technical support center, the emergency operations facility, and operations support center during an

emergency preparedness drill conducted on October 11, 2005. The inspection focused

on the ability of the licensee to appropriately classify emergency conditions, complete

timely notifications, and implement appropriate protective action recommendations in

accordance with approved procedures.

This review represented one inspection sample.

b. Findings

No findings of significance were identified.4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

Cornerstone:

Emergency Preparedness The inspectors reviewed the licensee's records associated with the three EP performance indicators (PIs) listed below. The inspectors verified that the licensee accurately reported

these indicators in accordance with relevant procedures and Nuclear Energy Institute

guidance endorsed by the NRC. Specifically, the inspectors reviewed licensee records

associated with PI data reported to the NRC for the period July 2004 through September

2005. Reviewed records included procedural guidance on assessing opportunities for the

three PIs; assessments of PI opportunities during pre-designated Control Room

Simulator training sessions, the 2004 biennial exercise, and other drills; revisions of the

roster of personnel assigned to key ERO positions; and results of periodic Alert and

Notification System (ANS) operability tests. The following PIs were reviewed:*ANS;*ERO Drill Participation; and

  • Drill and Exercise Performance.

These activities represented three inspection samples.

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152).1Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine whether they

were being entered into the licensee's corrective action program at an appropriate

threshold, that adequate attention was being given to timely corrective actions, and that

adverse trends were identified and addressed.

This is not an inspection sample.

b. Findings

No findings of significance were identified..2Annual Sample Review - 10 CFR 50.59 Review

a. Inspection Scope

As discussed in NRC Inspection Report 05000440/2005003, dated July 8, 2005, a finding of very low safety significance and an associated NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," was NRC-identified when licensee personnel failed to

adequately address a nonconforming condition in the design of the EDGs. This condition

made the EDGs vulnerable to damage in response to a loss of offsite power (LOOP)

signal under certain scenarios. The licensee contested this violation by letter dated

August 8, 2005, with one of the reasons given that a LOOP start was not an "emergency"

start. During NRC followup of the contested violation, the NRC requested the safety

evaluation associated with PNPP [Perry Nuclear Power Plant] Change Request 88-127, dated December 17, 1988, which revised the wording for Final Safety Analysis Report (FSAR) Section 8.3.1.1.3.2.b.7(e) from "emergency start signal" to "LOCA [Loss of

Coolant Accident] start signal." Following that request, licensee personnel were unable to

locate either the change request or the safety evaluation for this change and generated

CR 05-06193 "USAR Change Request and 10 CFR 50.59 Review Paperwork Could Not

Be Located," to document this issue. By letter dated September 7, 2005, the NRC

disputed the licensee's denial of NCV 05000440/2005003-14 because the NRC found

that a LOOP signal was, in fact, an emergency start signal, as was stated in numerous

other FSAR/Updated Safety Analysis Report (USAR) sections.

After further review, the licensee located Change Request 88-127 and Safety Evaluation 88-179; the 10 CFR 50.59 review package referenced in CR 05-06193.

23 On September 14, 2005, the licensee initiated CR 05-06622, "NRC Denial of Disputed NCV 2005003-14 (EDG Design Basis Issue)," to address the design changes to be

implemented to address the start of the EDGs during the first 2 minutes following an

engine shutdown. In CR 05-06622, the licensee noted that Change Request 88-127 had

been evaluated as an administrative change rather than a technical change; therefore, the 10 CFR 50.59 review may have been inadequate. The licensee initiated

CR 05-07104, "Inadequate 10 CFR 50.59 Evaluation of USAR Change," on

October 12, 2005, to document the issue. CR 05-07104 was closed to the investigation

and corrective actions associated with CR 05-06622, since this CR would direct any

necessary changes to bring the EDG starting signal back into compliance with the USAR.

The licensee initiated an action to prepare an engineering change to correct the EDGs

failure to start from an under-voltage, or a degraded voltage signal from an associated

bus, during the 2 minutes after an engine shutdown. In CR 05-06622, the licensee

completed a technical review of Safety Evaluation 88-179, which found the evaluation to

be correct.

The inspectors selected CR 05-06193, "USAR Change Request and 10 CFR 50.59 Review Paperwork Could Not Be Located," dated August 23, 2005, for detailed review.

This review represented one inspection sample.

b. Findings and Observations

No findings of significance were identified.

The inspectors reviewed the licensee's 10 CFR 50.59 evaluation, including Change Request 88-127 and Safety Evaluation 88-179, and determined that since the USAR

section being revised was strictly associated with the response of an EDG to a LOCA

signal, the change was appropriate. However, the inspectors also noted, as was

identified in other sections of the USAR, the EDGs are required to automatically start

upon receipt of a signal other than a LOCA signal, such as an under-voltage signal, or a

degraded voltage signal from the EDG's associated bus.

Therefore, the inspectors concluded that although the licensee's 10 CFR 50.59 evaluation was adequate and the licensee's evaluations in CR 05-6622 were correct

when limited to USAR Section 8.3.1.1.3.2.b.7; the overall starting requirements for the

EDGs were more extensive, as was reflected in other sections of the USAR..3Semi-Annual Trend Review a.The inspectors reviewed monthly performance reports, self-assessments, quality assurance assessment reports, performance im provement initiatives and CRs to identify any trends that had not been adequately evaluated or addressed by proposed corrective

actions.These reviews did not constitute an inspection sample. b .Findings 24 No findings of significance were identified..4Problem Identification and Resolution Biennial Review This review was completed by reference during the Perry IP 95003 supplemental inspection conducted from January through May 2005 and documented in NRC

Inspection Report 05000440/2005003.4OA3Event Followup (71153).1(Closed) Licensee Event Report (LER) 2005-03-00

Lack of Suction Path Causes High Pressure Core Spray to be Inoperable. A discussion of this event, and an associated

licensee-identified NCV, is contained in Section

4OA7 of this report.

This review represented the first of two samples for this inspection procedure..2Reportable Events and Configuration Control Issues During Scheduled Division 1 Maintenance Outage On November 3 and November 4, 2005, the licensee responded to several emergent configuration control issues associated with plant safety systems. The issues included:

(1) a tagout that inadvertently rendered a nuclear closed cooling containment isolation

valve as well as the 'A' annulus exhaust gas treatment system inoperable;

(2) a breaker found open that affected the operability of the 'A' emergency service water remote

shutdown system; and

(3) a breaker found open associated with the 'A' standby liquid

control system. The inspectors observed the licensee response and reviewed the

licensee's actions to determine compliance with licensee procedures, TS, and the

reporting requirements of 10 CFR 50.72. Two violations of very low safety significance (Green) were identified by the licensee and are documented in Section

4OA7 of this

report.This review represented the second of two inspection samples for this inspection procedure.4OA5Other (71114.03)

Use of Adjustment Factors to Meet ERO Staffing Timeliness Goals (URI 05000440/2005003)

The inspectors discussed with licensee staff the Perry IP 95003 supplemental inspection report, which identified an unresolved item (URI) regarding the use of adjustment factors

to meet ERO staffing timeliness goals. The inspectors advised the licensee that this

issue will continue to be evaluated during the follow-up to the IP 95003 Supplemental

Inspection early in 2006.

This is not an inspection sample.4OA6Meetings 25.1Exit Meeting On January 6, 2006, the resident inspectors presented the inspection results to Mr. W. Pearce, Acting Vice President, and other members of his staff who acknowledged

the findings.

The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified..2Interim Exit Meetings Exit meetings were conducted for:

  • Operator Requalification Program Examination Result Review with Mr. W. O'Malley on December 16, 2005 by telephone.*Emergency Preparedness inspection with Messrs. W. Pearce, R. Anderson, F. von Ahn, and other members of licensee management on December 9, 2005.

A telephone exit was held on December 16, 2005, with Messrs. V. Higaki, Fleet

Operations Manager; and L. Burgwald, Emergency Preparedness Senior

Specialist.4OA7Licensee-Identified Violations The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

Cornerstone:

Barrier Integrity

  • Technical Specification 5.4, "Procedures," required the implementation of the applicable procedures recommended in Regulatory Guide 1.33, "Quality

Assurance Program Requirements (Operation)," Revision 2, dated February 1978.

Regulatory Guide 1.33, Appendix A, Part 1.c, recommended procedures for

equipment control. Contrary to this requirement, on November 3, 2005, licensee

personnel failed to control the impact of a clearance that removed logic fuses

associated with Group 2A containment isolation valves and failed to enter

numerous required TS action statements. The licensee entered the issue into

their corrective action program as CR 05-07442. The inspectors determined that

the issue was of very low safety significance because it:

(1) did not represent a

degradation of the barrier function of the control room against smoke or toxic

atmosphere; and

(2) did not represent an actual open pathway in the physical

integrity or reactor containment, or involve an actual reduction in defense-in-depth

for the atmospheric pressure control or hydrogen control functions of the reactor

containment.

Cornerstone:

Mitigating Systems 26Technical Specification 5.4, "Procedures," required the implementation of the applicable procedures recommended in Regulatory Guide 1.33, "Quality

Assurance Program Requirements (Operation)," Revision 2, dated February 1978.

Regulatory Guide 1.33, Appendix A, Paragraph 4, required procedures for the

operation of safety-related boiling water reactor systems. Similarly, Paragraph

8.b.(2)(j) required specific procedures for ECC system surveillance tests.

Contrary to this requirement, on September 20, 2005, licensee personnel

identified that SVI-E22-T2001, "HPCS [High Pressure Core Spray] Pump and

Valve Operability Test," Revision 17, prescribed steps that simultaneously closed

both HPCS suction valves without HPCS being declared inoperable. The licensee

subsequently identified that SOI-E22A, "High Pressure Core Spray System,"

Revision 13, prescribed steps in the HPCS system operating instruction for

swapping the suction source from the suppression pool to the condensate storage

tank that resulted in the same condition. The licensee determined that an

inadvertent manual start or non-time-del ayed automatic start of the HPCS pump with both suction valves closed could pr event the HPCS system from performing its intended function or could result in equipment damage. Licensee log reviews

estimated that the system was in this vulnerable configuration (no aligned suction

source) for about 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> over the past 3 years. Licensee personnel determined

that the primary cause of the event was a personnel knowledge deficiency and

inadequate procedural guidance.

The inspectors determined the issue was more than minor in that the unrecognized system inoperability was related to the maintenance risk

assessment and risk management issues specified in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports," dated

September 30, 2005. The inspectors performed a Phase 1 review in accordance

with Appendix A, "Determining the Significance of Reactor Inspection Findings for

At-Power Situations," of IMC 0609, "Significance Determination Process (SDP),"

dated November 22, 2005. The inspectors determined that a Phase 2 review was

required because the finding represented a loss of system safety function. The

inspectors conducted a Phase 2 review and determined that a Phase 3 review

was required. The Region III Senior Reactor Analyst performed a Phase 3

evaluation of the finding assuming that the HPCS pump was unavailable for

14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />. The Perry Simplified Plant Analysis Risk (SPAR) analysis, Revision 3.21, was used to perform the evaluation. The result was a change in

core damage frequency (CDF) significantly less than 1E-6. The dominant

sequence involved a loss of offsite power, failure of the emergency power system, failure of the HPCS system, and the failure to recover offsite power. As such, the

finding was determined to be of very low safety significance. The licensee

entered this finding into their corrective action program as CR 05-6751.Technical Specification 5.4, "Procedures," required the implementation of the

applicable procedures recommended in Regulatory Guide 1.33, "Quality

Assurance Program Requirements (Operation)," Revision 2, dated February 1978.

Regulatory Guide 1.33, Appendix A, Part 1.c., recommended procedures for

equipment control. Contrary to this requirement, on November 3, 2005, licensee

personnel identified that a breaker affecting the ESW 'A' remote shutdown 27 ventilation system was incorrectly left in the open position. The licensee determined that a clearance restoration incorrectly restored the breaker to the "off"

position on March 27, 2005. This breaker affected the back-up control power

required to be available for the 'A' ventilation train. For a control room fire hot

short scenario, if power had been selected to the back-up source, the ESW

ventilation system would have shut down and the ESW pumphouse could have exceeded its maximum operating temperature. The licensee restored the breaker

on November 3, 2005, and entered the issue into their corrective action program

as CR 05-07435. The inspectors used Appendix F, "Fire Protection Significance

Determination Process," dated February 28, 2005 of IMC 0609, "Significance

Determination Process," dated November 22, 2005, to assess the significance.

The inspectors determined that the issue was of very low safety significance

because it was categorized as a "Cold Shutdown" finding per Step 1.1 and was

bounded by Step 1.3 in that it only affected the ability to reach and maintain cold

shutdown conditions.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

W. Pearce, Acting Vice President
F. von Ahn, General Manager, Nuclear Power Plant Department
R. Anderson, Vice President, Operations
N. Bonner, Manager, Perry Oversight
F. Cayia, Director, Performance Improvement
K. Cimorelli, Manager, Work Management
V. Higaki, Manager, Fleet Operations
J. Lausberg, Manager, Regulatory Compliance
T. Lentz, Director, Performance Improvement Initiative
J. Messina, Manager, Operations
J. Shaw, Director, Engineering
M. Wayland, Maintenance Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000440/2005010-01NCVInadequate Fuel Oil Pump Procedures Resulted in Division 2

EDG Unavailability (Section 1R19.1)05000440/2005010-02NCVInadequate Oil Reservoir Maintenance Procedure

Implementation for ECC 'B' Pump Resulted In Oil Leak

(Section 1R19.2)05000440/2005010-03NCVFailure to Correct an Oil Reservoir Maintenance Procedure

Issue Resulted In ECC 'A' Oil Leak (Section 1R19.3)

Closed2005-03-00LERLack of Suction Path Causes High Pressure Core Spray to

be Inoperable (Section 4OA3)

Discussed

05000440/2005003-01URIUse of Adjustment Factors to Meet ERO Staffing

Timeliness Goals (Section 4OA5)

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection.

Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort.

Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

IOI-15; Seasonal Variations; Revision 7
ONI-R36-2; Extreme Cold Weather; Revision 1
PTI-GEN-P0026; Preparations for Winter Operation; Revision 2
PTI-GEN-P0027; Cold Weather Support System Startup; Revision 7
PTI-GEN-P0027; Cold Weather Support System Startup; Revision 8
SOI-R36; Heat Trace and Freeze Protection System; Revision 6
SOI-P45/49; Emergency Service Water and Screen Wash Systems; Revision 11

Section 1R04: Equipment Alignment

VLI-P47; Control Complex Chilled Water System; Revision 6
SOI-P47; Control Complex Chilled Water System; Revision 13
VLI-R47; Division 1 and 2 Diesel Generator Lube Oil; Revision 5
VLI-R44; Division 1 and 2 Diesel Generator Starting Air System (Unit 1); Revision 4
VLI-R48; Division 1 and 2 Diesel Generator Exhaust, Intake and Crankcase Systems; Revision 6
VLI-R46; Division 1 and 2 Diesel Generator Jacket Water Systems (Unit 1); Revision 3
VLI-R45; Division 1 and 2 Diesel Generator Fuel Oil System (Unit 1); Revision 4
WO 200161353; Level Element for Division 1 EDG Fuel Oil Storage Tank; dated July 21, 2005

Section 1R05: Fire Protection

FPI-1DG; Diesel Generator Building; Revision 4
FPI-TB; Turbine Building; Revision 2
FPI-HB; Heater Bay; Revision 1
FPI-1AB; Auxiliary Building Unit 1; Revision 2

Section 1R07: Heat Sink

WO 200150844; RHR Exchangers 'A' And 'C' Performance Testing; dated December 1, 2005
PTI-E12-P0002; RHR Heat Exchanger 'A' and 'C' Performance Testing Trend Chart; dated
December 20, 2000

Section 1R12: Maintenance Effectiveness

CR 05-06331; Incorrect Functional Location in Order; dated August 30, 2005
CR 05-05822; RFA [Request for Assistance] - As Found Contact Resistance High; dated
August 3, 2005
CR 05-05697; WO Given to Operations for Restoration Prior to Post Maint Requirements Completion; dated July 28, 2005
CR 05-05560; PCR [Procedure Change Request] - Deficiency
ONI-R42-5; dated July 23, 2005
CR 05-04861; Bus
ED-2-C Ground Detection; dated June 16, 2005
CR 05-04567; Category "A" Limits Not Met on Unit 1 Division 2; dated May 31, 2005
CR 05-02416;
ED-1-B Ground Alarm in Control Room; dated March 16, 2005
CR 05-01350; Loss of D1B07; dated February 23, 2005
CR 05-05622; Evaluate NRC Information Notice 2005-21 - Switchyard Maintenance
Issues/Effects; dated July 26, 2005
CR 05-05500; Fleet Focused Self-Assessment On Switchyard, Transformer & Grid Reliability;

dated July 21, 2005

CR 05-03354; OE19195 - Switchyard Disconnect Switches Indicate Higher Than Normal
Temperature; dated April 13, 2005
CR 05-02232; Inadequate Communication of Changes in Transmission Switchyard Work; dated
March 14, 2005
CR 05-02046; PII [Performance Improvement Init iative] B Work Management Action: Improve Program Interface with Switchyard Work; dated March 10, 2005
CR 04-02014; RCIC Turbine Exhaust Pressure Runs High; dated April 19, 2004
CR 04-02384; Leakage Identified Associated with RCIC System; dated May 11, 2004
CR 04-03680; 1E51F0022 Failed to Meet its Stroke Time Close; dated July 15, 2004
CR 04-03721; RCIC Governor Valve Stuck During
SVI-E51T2001; dated July 17, 2004
CR 04-03789; Reactor Core Isolation Cooling Periodic Maintenance/Test Scope/Frequency
Review; dated July 20, 2004
CR 04-05756; PII Latent Issues Review Identified 1E51F015 Not Tested or Maintained; dated
November 2, 2004
CR 04-05790; PII Latent Issues RCIC Review - USAR Table 6.2-32 Update; dated
November 4, 2004
CR 04-05975; PII LIR Calculation
ECA-068 Assumption Not Justified; dated November 16, 2004
CR 04-06169; RCIC System Walkdown Deficiency; dated November 10, 2004
CR 04-06252; Planned Performance of Testing on Protected Equipment (RCIC) During Div 1
Outage; dated November 29, 2004

Section 1R13:

Maintenance Risk Assessments and Emergent Work Control On-Line Probabilistic Safety Assessment; Week 11, Period 2; Revision 2
PAP [Perry Administrative Procedure] -1924; Risk-Informed Safety Assessment and Risk
Management; Revision 4
Main Condenser Leak Downpower Schedule; dated October 12, 2005
On-Line Probabilistic Safety Assessment; Week 12, Period 2; Revision 1
Perry Work Implementation Schedule; Week 7, Period 3

Section 1R14: Operator Performance During Non-routine Evolutions and Events

ONI [Off-Normal Instruction] -N61; Condenser Tube Leak/Organic Intrusion; Revision 9
REC-0104; Chemistry Specifications; Revision 15
SOI [System Operating Instruction] -N71; Circulating Water/Condenser Mechanical Cleaning
System; Revision 11
5

Section 1R15: Operability Evaluations

CR 05-07098; Division 1 Diesel Left Bank 4 Cylinder Has Jacket Water Leakage; dated October 5, 2005
CR 01-0531; Diesel Generator Jacket Water Leakage; dated February 15, 2001
Calculation R46T03; NonSafety-Related Setpoint Tolerance Calculation for 1R46N0062A(B)
Diesel Jacket Water Stand Pipe Water Level; Revision 3
CR 04-02772; Division 2 Jacket Water Keepwarm Pump Leak; dated May 27, 2004
CR 05-07314; Sensitivity and Timely Response on Lower Level Issues Associated with Safety-
Related Equipment; dated October 26, 2005
CR 05-07467; Diesel Hallway Insulation Unistrut Loose Bolt; dated November 6, 2005
CR 05-07340; 3 Loose Fasteners in DG Exhaust Ha llway Near Construction Opening; dated October 27, 2005

Section 1R16: Operator Workarounds

CR 05-05079; Benchmarking Trip to Monticello Nuclear Power Plant Report; dated June 29, 2005
CR 05-05605; M&C 14, Work Arounds Policy, is Not Effective; dated July 25, 2005
CR 05-05867; 2

nd Quarter Assessment of Control Room Deficiencies, Work Arounds, and Burdens; dated August 8, 2005

CR 05-06962; Operator Workarounds Dropped at T+10 Due to Uncompleted ECP; dated
September 30, 2005
List of Operator Burdens; dated October 4, 2005

Section 1R19: Post-Maintenance Testing

WO 200138847; Calibration Check for OM26N0711A; dated October 6, 2005
WO 200097190; Control Room Emergency Recirculation A; dated October 5, 2005
WO 200138846; Calibration Check for OM26N0708A; dated October 6, 2005
WO 200134210; Control Room Emergency Recirculation A PMT; dated October 6, 2005
FTI-F0036; Post-Maintenance Test Manual; Revision 3
WO 200173745; Replace S8 on 1H13P877; dated October 18, 2005
PTI-R43-P0006-A; Division 1 Diesel Generator Pneumatic Logic Board Functional Check;
Revision 5
CR 05-07511; Failure of a Newly Installed Pneumatic Logic Board for Division 1 Diesel
Generator; dated November 8, 2005
CR 05-07505; Procedure Errors in
PTI-R43P0006A; dated November 9, 2005
PMI-0050; Preventative Maintenance Lubricating Guidelines; Revision 3
WO 200188113; Emergency Closed Cooling Pump Outboard Bearing Oil Bubbler; dated
November 29, 2005
CR 05-07371; ECC Pump 1P42C0001B Outboard Pump Bearing Oil Leak; dated
October 29, 2005
CR 05-07383; Oil Leak on Outboard Oil Seal; dated October 31, 2005
CR 05-07379; Failed PMT for ECC B; dated October 31, 2005
CR 05-07404; Operability Determination Extension Requested; dated October 31, 2005
CR 05-07685; Emergency Closed Cooling Pump A Inboard Bearing Bubbler Adjustment; dated
November 19, 2005
WO 200187088; ECC Pump A Bubbler Rework; dated November 28, 2005
WO 200146833; ECC Pump A Bubbler Replacement; dated November 5, 2005
WO 200075252; ECC Pump B Maintenance and Bubbler Replacement; dated
September 14, 2005
CR 05-07633; TBCC Pump A Failed PMT [Post Maintenance Test]; dated November 16, 2005
CR 05-07683; TBCCW Pump A - Failed PMT/Repeat Maintenance; dated November 19, 2005

Section 1R22: Surveillance Testing

SVI-C71-T0039; MSIV [Main Steam Isolation Valve] Closure Channel Functional; Revision 6
SVI-P47-T2001-B; Control Complex Chilled Water B Pump and Valve Operability Test;
Revision 3
SVI-C61-T1201; Remote Shutdown Panel 1C61-P001 Control Operability Test RHR A, ESW A, And ECC A; Revisions 1, 2, 3, and 4
SVI-E22-T2001; HPCS Pump and Valve Operability Test; Revision 18
CR 05-07711; NRC Procedural Concern During Performance of
SVI-C61-T1201; dated
November 22, 2005
SVI-R43-T1317; Diesel Generator Start and Load Division 1; Revision 12

Section 1R23:

Temporary Plant Modifications Alternate Diesel Generator Starting Air Supply Temporary Modification; dated November 4, 2005

Section 1EP2:

Alert and Notification System (ANS) Testing The Siren Alerting System for the Perry Nuclear Power Plant; dated June 1985
Perry Prompt Alert Siren System History; dated 1996 through 2005
PSI-0021; Prompt Alert System; dated September 9, 2005
Letter from FEMA [Federal Emergency Management Agency] to NRC; Perry Prompt Alert and Notification System Approval Letter; dated September 8, 1986
PNPP [Perry Nuclear Power Plant] 6813; Prompt Alert System Annual Maintenance Checklist;

dated June 28 through October 14, 2004

PNPP 6814; Prompt Alert System Maintenance Checklist; dated November 12 through
December 17, 2004, and May 15 through June 24, 2005
PNPP 6817; Perry Plant Prompt Alert System Repair Report; dated October 4, 2004 through
September 24, 2005
2004 Emergency Planning Zone Siren System Test Schedule
CR 05-04947; Lake County Siren Activation Failure; dated June 20, 2005

Section 1EP3:

Emergency Response Organization (ERO) Augmentation Testing Perry Emergency Plan; Section 6.1; Activa tion of Emergency Organizations; Revision 24
Perry Emergency Plan; Section 8.8.4; Frequency of Drills and Exercises; Revision 24
EPI-B1; Form PNPP 9100; Emergency Notification System Pager Messages; Revision 17
PSI-0016; Testing of Plant Support Callout Scenarios; Revision 2
PSI-0022; Attachments 1 and 2; Emergency Plan Training Program Course Listing and
Requirements; Revision 0
PTI-GEN-P0003; Quarterly Testing of the Emergency Pager System; Revision 6
771PYRC2005; ERO [Emergency Response Organization] Off Hours Unannounced Drill Self-Assessment Report, dated August 19, 2005
759PYRC2005; ERO Off Hours Unannounced Drill Self-Assessment Report; dated
June 10, 2005
24PYRC2004; ERO Off Hours Unannounced Drill Self-Assessment Report; dated
November 18, 2004
2RAS2004; ERO Off Hours Unannounced Drill Self-Assessment Report; dated April 2, 2004
Perry Emergency Telephone Directory; Revision 2005-3/4
Integrated On Call Report for Emergency Response Organization; dated December 7, 2005
CR 05-07966; Two Radiation Protection Individuals' Qualifications Indicate Past Due and They

are Still in the Emergency Telephone Directory; dated December 8, 2005

CR 05-06260; Lapsed Emergency Response Organization Qualifications; dated August 25, 2005

Section 1EP4:

Emergency Action Level and Emergency Plan Changes Emergency Plan for Perry Nuclear Power Plant; Revision 23
Emergency Plan for Perry Nuclear Power Plant; Revision 22
Emergency Plan for Perry Nuclear Power Plant; Revision 21

Section 1EP5: Correction of Emergency Preparedness Weaknesses and Deficiencies

IPA 764PYRC2005; First Half 2005 Integrated Performance Assessment; dated August 2, 2005
PY-C-05-03; Perry Nuclear Quality Oversight Assessment Quarterly Audit Report; dated
November 23, 2005
PY-C-04-04; Perry Nuclear Quality Assessment Quarterly Audit Report; dated February 17, 2005
PY-C-04-03; Perry Nuclear Quality Assessment Quarterly Audit Report; dated November 5, 2004
PY-C-04-02; Perry Nuclear Quality Assessment Quarterly Audit Report; dated July 23, 2004
PY-C-04-01; Perry Nuclear Quality Assessment Quarterly Audit Report; dated April 23, 2004
PY-C-03-04; Perry Nuclear Quality Assessment Quarterly Audit Report; dated February 4, 2004
PY-C-03-03; Perry Nuclear Quality Assessment Quarterly Audit Report; dated October 22, 2003
PY-C-03-02; Perry Nuclear Quality Assessment Quarterly Audit Report; dated July 22, 2003
PY-C-03-01; Perry Nuclear Quality Assessment Quarterly Audit Report; dated March 19, 2003
753PYRC2005; June 20, 2005 ERO Team 'C' Training Drill Self-Assessment; dated
July 28, 2005
713RAS2004; October 5, 2004, ERO Team 'A' Ev aluated Exercise Self-Assessment Report;

dated November 4, 2004

CR 05-07313; CADAP Time Requirements in
EPI-A1 May Not Be Met Under All Circumstances;

dated October 26, 2005

CR 05-05657; Observation of Training EPlan TSC [Technical Support Center] Operation
Manager Overall Unsat Rating; dated July 27, 2005
CR 05-04753;
RIS 2005-08 Endorsement NEI [Nuclear Energy Institute] Guidance for Sheltering
Protective Action Recommendations; dated June 9, 2005
CR 05-00107; PII B Re-Examine Respiratory Protection Qualification for ERO; dated
January 6, 2005
CR 04-05953; CO2 System Actuation Results in Emergency Plan Entry; dated
November 12, 2004

Section 1EP6: Drill Evaluation

Controller's Handbook; Team "A" ERO Drill; dated October 11, 2005

Section 4OA1:

Performance Indicator (PI) Verification Perry Emergency Plan; Section 7.4; Prompt Alert Siren System; Revision 24
PYBP-RAS-0004; Appendix A; NRC Performance Indicators; Emergency Response Organization
Drill Participation; Revision 1
PYBP-RC-0004; Figure 1(l); NRC Performance Indicators; ERO Drill Participation, Document

and Data Review Form; dated July 2004 through September 2005

PYBP-RAS-0004; Appendix A; NRC Performance Indicators; ERO Drill/Exercise Performance;
Revision 2
PYBP-RC-0004; Figure 1(k); NRC Performance Indicators; Emergency Preparedness
Drill/Exercise Performance; Document and Data Review Form; dated July 2004 through
September 2005
PYBP-EPU-0028; Prompt Alert Siren System Emergency Planning Zone Testing; Revision 1
PYBP-RC-0004; Figure 1(m); NRC Performance Indicators; Alert and Notification System
Reliability; Document and Data Review Form; dated July 2004 through September 2005
PSI-0021; Attachment 3; Prompt Alert Syst em Siren Test Reports; dated July 2004 through September 2005
CR 05-07916; Credit Taken Incorrectly for Emergency Response Performance Indicator (DEP)

[Drill and Exercise Performance]; dated December 6, 2005

CR 05-06779; Alert and Notification System Reliability Indicator Reference Data Inaccurate;

dated September 21, 2005

Section 4OA2: Identification and Resolution of Problems

CR 05-07173; Declining Site Performance Noted by CAP Predictive Trending; dated October 18, 2005
CR 05-07100; Declining Site Performance Noted by CAP Predictive Trending; dated
October 11, 2005
CR 05-06994; September Cognitive Trending for Maintenance Section - Work Package Errors;

dated October 4, 2005

CR 05-06216; Cognitive Trend of T+6 Meeting Observations Deemed Unsatisfactory; dated
August 19, 2005
CR 05-06067; Containment Airlock Rework Trending; dated August 16, 2005
CR 05-06066; Declining Trend in Procedure Use and Adherence Issues Found During Section
IPA; dated August 16, 2005
CR 05-06065; Declining Trend in FME Issues Found During Section Integrated Performance
Assessment; dated August 16, 2005
CR 05-05650; Negative Trends Identified in Emergency Planning; dated July 27, 2005
Perry Nuclear Oversight Assessment Quarterly Audit Report
PY-C-05-01; dated May 31, 2005
Perry Nuclear Oversight Assessment Quarterly Audit Report
PY-C-05-02; dated August 19, 2005
9

Section 4OA3: Event Followup

LER [Licensee Event Report] 2005-003; Lack of Suction Flow Path Causes High Pressure Core Spray to be Inoperable; dated November 18, 2005
CR 05-07435; M32 A Breaker Found Open; dated November 3, 2005
CR 05-07442; Failure to Identify All Applicable TSs and Required Actions; dated
November 3, 2005

LIST OF ACRONYMS

USEDAN SAlert and Notification SystemCCCWcontrol complex chilled water
CFR Code of Federal Regulations

CRcondition reportDCdirect current

ECCemergency closed cooling

EDGemergency diesel generator

EPEmergency Preparedness

EPIemergency implementing procedures

EROEmergency Response Organization

ESWemergency service water

FPIFire Protection Instruction

FSARFinal Safety Analysis Report

FENOCFirstEnergy Nuclear Operating Company

HPCShigh pressure core spray

IMCInspection Manual Chapter

LERLicensee Event Report

NCVnon-cited violation

NRCNuclear Regulatory Commission

ONIOff-Normal Instruction

OWAoperator work around

PAPPerry Administrative Procedure

PIPerformance Indicator

PMIPreventive Maintenance Instruction

PMTpost-maintenance testing

RHRresidual heat removal

SDPsignificance determination process

SSCstructures, systems, and components

SVIsurveillance instruction

TBCCWTurbine Building Closed Cooling Water

TSTechnical Specification

USARUpdated Safety Analysis Report

VLIvalve lineup instruction

WO work order